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{{Adams|number = ML072120599}}
{{Adams
| number = ML072120599
| issue date = 07/30/2007
| title = IR 05000277-07-003, 05000278-07-003, 04/01/2007 - 06/30/2007, Peach Bottom Atomic Power Station (Pbaps), Units 2 & 3; Event Followup
| author name = Krohn P G
| author affiliation = NRC/RGN-I/DRP/PB4
| addressee name = Crane C M
| addressee affiliation = Exelon Generation Co, LLC, Exelon Nuclear
| docket = 05000277, 05000278
| license number = DPR-044, DPR-056
| contact person = KROHN P G, RI/DRP/PB4/610-337-5120
| document report number = IR-07-003
| document type = Inspection Report, Letter
| page count = 22
}}


{{IR-Nav| site = 05000277 | year = 2007 | report number = 003 }}
{{IR-Nav| site = 05000277 | year = 2007 | report number = 003 }}


=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION I475 ALLENDALE ROADKING OF PRUSSIA, PENNSYLVANIA 19406-1415  July 30, 2007 Mr. Christopher President and CNO Exelon NuclearExelon Generation Company, LLC200 Exelon Way Kennett Square, PA 19348
[[Issue date::July 30, 2007]]


Mr. Christopher M. CranePresident and CNOExelon NuclearExelon Generation Company, LLC200 Exelon Way Kennett Square, PA 19348
SUBJECT: PEACH BOTTOM ATOMIC POWER STATION - NRC INTEGRATED INSPECTION REPORT 05000277/2007003 AND 05000278/2007003
 
SUBJECT: PEACH BOTTOM ATOMIC POWER STATION - NRC INTEGRATEDINSPECTION REPORT 05000277/2007003 AND 05000278/2007003


==Dear Mr. Crane:==
==Dear Mr. Crane:==
On June 30, 2007, the United States Nuclear Regulatory Commission (NRC) completed aninspection at your Peach Bottom Atomic Power Station (PBAPS), Units 2 and 3. The enclosedintegrated inspection report documents the inspection results, which were discussed on July 20, 2007, with Mr. J. Grimes and other members of your staff.The inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewedpersonnel. The report documents three self-revealing findings of very low safety significance (Green). Two ofthese findings were determined to involve violations of NRC requirements. Additionally, threelicensee-identified violations which were determined to be of very low safety significance are listedin this report. However, because of the very low safety significance and because they are entered into your corrective action program (CAP), the NRC is treating these findings as non-citedviolations (NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contestany NCV in this report, you should provide a response within 30 days of the date of this inspectionreport, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: DocumentControl Desk, Washington, D.C. 20555-0001; with copies to the Regional Administrator, Region I;the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington,D.C. 20555-0001; and the NRC Resident Inspector at Peach Bottom.
On June 30, 2007, the United States Nuclear Regulatory Commission (NRC) completed aninspection at your Peach Bottom Atomic Power Station (PBAPS), Units 2 and 3. The enclosedintegrated inspection report documents the inspection results, which were discussed on July 20, 2007, with Mr. J. Grimes and other members of your staff.The inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. The report documents three self-revealing findings of very low safety significance (Green). Two ofthese findings were determined to involve violations of NRC requirements. Additionally, threelicensee-identified violations which were determined to be of very low safety significance are listedin this report. However, because of the very low safety significance and because they are entered into your corrective action program (CAP), the NRC is treating these findings as non-citedviolations (NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contestany NCV in this report, you should provide a response within 30 days of the date of this inspectionreport, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: DocumentControl Desk, Washington, D.C. 20555-0001; with copies to the Regional Administrator, Region I;the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington,D.C. 20555-0001; and the NRC Resident Inspector at Peach Bottom.


C. M. Crane2In accordance with 10 Code of Federal Regulations (CFR) 2.390 of the NRC's "Rules of Practice,"a copy of this letter, its enclosures, and your response (if any) will be available electronically forpublic inspection in the NRC Public Document Room or from the Publicly Available Records(PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from theNRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic ReadingRoom).
C. M. Crane2In accordance with 10 Code of Federal Regulations (CFR) 2.390 of the NRC's "Rules of Practice,"a copy of this letter, its enclosures, and your response (if any) will be available electronically forpublic inspection in the NRC Public Document Room or from the Publicly Available Records(PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from theNRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic ReadingRoom).


Sincerely,/RA/Paul G. Krohn, ChiefReactor Projects Branch 4Division of Reactor ProjectsDocket Nos.:50-277, 50-278License Nos.:DPR-44, DPR-56  
Sincerely,/RA/Paul G. Krohn, Chief Reactor Projects Branch 4Division of Reactor ProjectsDocket Nos.:50-277, 50-278License Nos.:DPR-44, DPR-56  


===Enclosures:===
===Enclosures:===
Line 24: Line 35:
Supplemental Informationcc w/encl:Chief Operating Officer, Exelon Generation Company, LLC Site Vice President, Peach Bottom Atomic Power Station Plant Manager, Peach Bottom Atomic Power Station Regulatory Assurance Manager - Peach Bottom Manager, Financial Control & Co-Owner Affairs Vice President, Licensing and Regulatory Affairs Senior Vice President, Mid-Atlantic Senior Vice President - Operations Support Director, Licensing and Regulatory Affairs J. Bradley Fewell, Assistant General Counsel, Exelon Nuclear Manager Licensing, PBAPS Director, Training Correspondence Control Desk Director, Bureau of Radiation Protection, Department of Environmental Protection R. McLean, Power Plant and Environmental Review Division (MD)
Supplemental Informationcc w/encl:Chief Operating Officer, Exelon Generation Company, LLC Site Vice President, Peach Bottom Atomic Power Station Plant Manager, Peach Bottom Atomic Power Station Regulatory Assurance Manager - Peach Bottom Manager, Financial Control & Co-Owner Affairs Vice President, Licensing and Regulatory Affairs Senior Vice President, Mid-Atlantic Senior Vice President - Operations Support Director, Licensing and Regulatory Affairs J. Bradley Fewell, Assistant General Counsel, Exelon Nuclear Manager Licensing, PBAPS Director, Training Correspondence Control Desk Director, Bureau of Radiation Protection, Department of Environmental Protection R. McLean, Power Plant and Environmental Review Division (MD)
G. Aburn, Maryland Department of Environment T. Snyder, Director, Air and Radiation Management Administration, MD Department of the Environment Public Service Commission of Maryland, Engineering Division Board of Supervisors, Peach Bottom Township B. Ruth, Council Administrator of Harford County Council Mr. & Mrs. Dennis Hiebert, Peach Bottom Alliance TMI - Alert (TMIA)
G. Aburn, Maryland Department of Environment T. Snyder, Director, Air and Radiation Management Administration, MD Department of the Environment Public Service Commission of Maryland, Engineering Division Board of Supervisors, Peach Bottom Township B. Ruth, Council Administrator of Harford County Council Mr. & Mrs. Dennis Hiebert, Peach Bottom Alliance TMI - Alert (TMIA)
J. Johnsrud, National Energy Committee, Sierra Club Mr. & Mrs. Kip Adams E. Epstein, TMI Alert R. Fletcher, Department of Environment, Radiological Health Program C. M. Crane2In accordance with 10 Code of Federal Regulations (CFR) 2.390 of the NRC's "Rules of Practice," a copy ofthis letter, its enclosures, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
J. Johnsrud, National Energy Committee, Sierra Club Mr. & Mrs. Kip Adams E. Epstein, TMI Alert R. Fletcher, Department of Environment, Radiological Health Program C. M. Crane2In accordance with 10 Code of Federal Regulations (CFR) 2.390 of the NRC's "Rules of Practice," a copy ofthis letter, its enclosures, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/r eading-rm/adams.html (the Public Electronic Reading Room).


Sincerely,/RA/Paul G. Krohn, ChiefReactor Projects Branch 4 Division of Reactor ProjectsDocket Nos.:50-277, 50-278License Nos.:DPR-44, DPR-56  
Sincerely,/RA/Paul G. Krohn, Chief Reactor Projects Branch 4 Division of Reactor ProjectsDocket Nos.:50-277, 50-278License Nos.:DPR-44, DPR-56  


===Enclosures:===
===Enclosures:===
Line 33: Line 44:
===w/Attachment:===
===w/Attachment:===
Supplemental InformationDistribution w/encl:S. Collins, RAR. Fuhrmeister, DRP M. Dapas, DRAT. Setzer, DRP J. Lamb, RI OEDO F. Bower, DRP - Senior Resident Inspector H. Chernoff, NRRM. Brown, DRP - Resident Inspector J. Hughey NRR, PMS. Schmitt - Resident OA P. Bamford, PM, BackupRegion I Docket Room (with concurrences)
Supplemental InformationDistribution w/encl:S. Collins, RAR. Fuhrmeister, DRP M. Dapas, DRAT. Setzer, DRP J. Lamb, RI OEDO F. Bower, DRP - Senior Resident Inspector H. Chernoff, NRRM. Brown, DRP - Resident Inspector J. Hughey NRR, PMS. Schmitt - Resident OA P. Bamford, PM, BackupRegion I Docket Room (with concurrences)
J. Lubinski, NRRROPreports@nrc.govP. Krohn, DRP SUNSI Review Complete: __PGK_______ (Reviewer's Initials)DOCUMENT NAME: C:\FileNet\ML072120599.wpdAfter declaring this document "An Official Agency Record" it will be released to the Public.To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" =Copy with attachment/enclosure "N" = No copyML072120599OFFICERI/DRP Rl/DRP NAMEFbower/PGK forPKrohn/PGKDATE07/24/0707/24/07OFFICIAL RECORD COPY U. S. NUCLEAR REGULATORY COMMISSIONREGION IDocket Nos.:50-277, 50-278 License Nos.:DPR-44, DPR-56 Report No.:05000277/2007003 and 05000278/2007003 Licensee:Exelon Generation Company, LLC Facility:Peach Bottom Atomic Power Station (PBAPS), Units 2 and 3 Location:Delta, Pennsylvania Dates:April 1, 2007 through June 30, 2007 Inspectors:F. Bower, Senior Resident InspectorM. Brown, Resident Inspector R. Fuhrmeister, Senior Project Engineer R. Nimitz, Senior Health Physicist N. Perry, Sr. Emergency Response Coordinator R. Cureton, Emergency Preparedness InspectorApproved by:Paul G. Krohn, ChiefReactor Projects Branch 4 Division of Reactor Projects ii
J. Lubinski, NRRROPreports@nrc.govP. Krohn, DRP SUNSI Review Complete: __PGK_______ (Reviewer's Initials)DOCUMENT NAME: C:\FileNet\ML072120599.wpdAfter declaring this document "An Official Agency Record" it will be released to the Public.To receive a copy of this document, indicate in the box:  
" C" = Copy without attachment/enclosure " E" =Copy with attachment/enclosure " N" = No copyML072120599OFFICERI/DRP Rl/DRP NAMEFbower/PGK forPKrohn/PGKDATE07/24/0707/24/07OFFICIAL RECORD COPY U. S. NUCLEAR REGULATORY COMMISSIONREGION IDocket Nos.:50-277, 50-278 License Nos.:DPR-44, DPR-56 Report No.:05000277/2007003 and 05000278/2007003 Licensee:Exelon Generation Company, LLC Facility:Peach Bottom Atomic Power Station (PBAPS), Units 2 and 3 Location:Delta, Pennsylvania Dates:April 1, 2007 through June 30, 2007 Inspectors:F. Bower, Senior Resident InspectorM. Brown, Resident Inspector R. Fuhrmeister, Senior Project Engineer R. Nimitz, Senior Health Physicist N. Perry, Sr. Emergency Response Coordinator R. Cureton, Emergency Preparedness InspectorApproved by:Paul G. Krohn, ChiefReactor Projects Branch 4 Division of Reactor Projects ii


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
.....................................................iii
IR 05000277/2007-003, 05000278/2007-003; 04/01/2007 - 06/30/2007; Peach Bottom AtomicPower Station (PBAPS), Units 2 and 3; Event Followup. The report covered a 3-month period of inspection by resident inspectors, a senior projectengineer, and announced inspections by a senior health physicist, a senior emergency response coordinator, and an emergency preparedness inspector. Three Green findings, two of which were NCVs, were identified. The significance of most findings is indicated by their color (Green,
White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006. A.
 
===NRC-Identified and Self-Revealing Findings===
 
===Cornerstone: Mitigating Systems===
: '''Green.'''
A self-revealing finding was identified for inadequate implementation ofwork order (WO) instructions to verify the correct breaker frame size during the overhaul of a compatible spare breaker for installation into the '4T4' 480 volt load center. This condition resulted in a poor electrical connection between the primary disconnect fingers and the switchgear bus stabs for one breaker in the '4T4' load center that ultimately resulted in a fire that led to a plant transient and declaration of an Unusual Event (UE).This finding is greater than minor because it affected the human performanceattribute of the Initiating Event Cornerstone, in that, an incorrect frame size breaker was installed into a cubicle for which it was not sized. This mismatch caused an electrical fault that led to a fire and a plant transient that upset plant stability. The finding was of very low safety significance (Green) because it did not increase both the likelihood of a reactor scram and that mitigation equipment or functions would not be available. The inspectors determined that this finding had a cross-cutting aspect in the area of human performance (work practices component) because maintenance technicians did not follow  WO instructions to specifically verify the frame size of a breaker during its overhaul  (IMC 0305 aspect H.4(b)). (Section 4OA3.1)*Green. A self-revealing NCV of Technical Specification (TS) 5.4.1, was identifiedwhen operators inadequately implemented a surveillance test by missing a procedure step. The missed step placed the E-3 emergency diesel generator (EDG) in the isochronous mode of operation while it was synchronized to off-site power and resulted in an unexpected over-loading of the E-3 EDG. This finding is more than minor because it was associated with the humanperformance attribute of the Mitigating Systems Cornerstone, and impacted the cornerstone objective of ensuring the availability of the E-3 EDG to respond to initiating events. This finding is of very low safety significance (Green) because all other EDGs remained operable and the actual loss of safety function of the E-3 EDG was less than the TS allowed outage time of seven days. The inspectors ivdetermined that this finding had a cross-cutting aspect in the area of humanperformance (work practices component) because PBAPS personnel did not follow procedures when the E-3 EDG was placed in the isochronous load control mode with the E-3 EDG in parallel with the off-site power source (IMC 0305 aspect H.4(b)). (Section 4OA3.2)*Green. A self-revealing NCV of TS 5.4.1, was identified when operatorsmanipulated a diesel-driven fire pump (DDFP) cooling water valve outside of procedure guidance. The improper manipulation led to misalignment of the DDFP cooling water that subsequently damaged the engine during operations without cooling water. The failure to use a procedure for cleaning and restoring the DDFP cooling waterstrainer was a more than minor finding because it was associated with the degradation of a fire protection feature, in that, the DDFP was rendered inoperable by damage to the engine. Using the Fire Protection SDP, the finding was determined to be of very low safety significance due to the motor-driven fire pump remaining operable during the five days the DDFP was inoperable, and the small number of fire scenarios which would impact the power supply to the motor-driven fire pump. This finding had a cross-cutting aspect in the area of human performance (resources component) because procedure ST-O-37D-340-2 did not provide complete and accurate instructions for cleaning the DDFP cooling water strainer (IMC 0305 aspect H.2©). (Section 4OA3.3)
 
===B.Licensee-Identified Violations===
Three violations of very low safety significance (Green), that were identified by thelicensee, have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's CAP. The violations and corrective actions are listed in Section 4OA7 of this report.
 
Enclosure


=REPORT DETAILS=
=REPORT DETAILS=
...........................................................1REACTOR SAFETY..........................................................11R01Adverse Weather Protection........................................11R04Equipment Alignment..............................................2
Summary of Plant StatusUnit 2 began the inspection period at 100 percent full rated thermal power (RTP) until April 27, 2007, when power was reduced to 58 percent for planned waterbox cleaning, control rod testing, 2 'A' reactor feed pump (RFP) maintenance, and other planned maintenance and testing. On April 28, 2007, the unit returned to full power where it remained until the end of the inspection period, except for brief periods to support planned testing and rod pattern adjustments. Unit 3 began the inspection period at 100 percent full RTP until April 16, 2007, when anunplanned power reduction to 84 percent was performed in response to rapidly increasing 3 'A' reactor recirculation pump shaft seal temperatures. The unit returned to full power on April 18, 2007. On May 4, 2007, power was reduced to 59 percent for planned waterbox cleaning, control rod testing, and 3 'C' RFP maintenance. The unit returned to full power on May 5, 2007. On May 11, 2007, power was reduced to 65 percent for a planned control rod pattern adjustment and RFP testing, and the unit returned to full power on May 12, 2007. On June 15, 2007, power was reduced to 82 percent for a rod pattern adjustment and planned maintenance on a feedwater heater drain line. The unit was returned to full power on June 16, 2007, where it remained until the end of the inspection period, except for brief periods to support planned testing and rod pattern adjustments.
 
==REACTOR SAFETY==
Cornerstones:  Initiating Events, Mitigating Systems, and Barrier Integrity1R01Adverse Weather Protection (71111.01 - 1 System Sample; 1 Site Sample).1Summer Seasonal Readiness


{{a|1R05}}
====a. Inspection Scope====
==1R05 Fire Protection...................................................3==
The inspectors performed one seasonal readiness sample that included a review of threeventilation systems. Specifically, the inspectors reviewed the procedures listed in 1 to the report, and verified summer ventilation system alignment for the diesel generator building, circulating water pump structure, and circulating water pump screen house.
 
====b. Findings====
No findings of significance were identified.
 
2Enclosure.2Adverse Weather Event Review
 
====a. Inspection Scope====
On June 13, 2007, a tornado warning was issued for an adjacent county. The inspectorsreviewed PBAPS's actions taken to respond to potential adverse environmental conditions from severe thunderstorms that entered the area. High winds, lightning, rain, and reports of hail were experienced at the site. The inspectors observed that PBAPS's personnel consulted procedure OP-PB-108-111-1001, "Preparation for Severe Weather," increased the online risk assessment to "Yellow," and subsequently implemented procedure AO 53.2-0, "Equipment Checks After a Thunderstorm."


{{a|1R11}}
====b. Findings====
==1R11 Licensed Operator Requalification Program.............................4==
No findings of significance were identified.
{{a|1R04}}
==1R04 Equipment Alignment (71111.04Q - 3 Partial Walkdown Samples).1Partial Walkdown==


{{a|1R12}}
====a. Inspection Scope====
==1R12 Maintenance Effectiveness.........................................41R13Maintenance Risk Assessments and Emergent Work Control...............51R15Operability Evaluations............................................51R19Post-Maintenance Testing..........................................61R22Surveillance Testing...............................................6==
The inspectors performed a partial walkdown of three systems to verify the operability ofredundant or diverse trains and components when safety-related equipment was inoperable. The inspectors performed walkdowns to identify any discrepancies that could impact the function of the system and potentially increase risk. The inspectors reviewed applicable operating procedures, walked down system components, and verified that selected breakers, valves, and support equipment were in the correct position to support system operation. The inspectors also verified that PBAPS had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the CAP. The three systems reviewed were: *E-3 Diesel Generator and 3 Startup Transformer with the 2 Startup TransformerOut-of-Service;*Unit 2 Reactor Core Isolation Cooling (RCIC) with Unit 2 High Pressure CoolantInjection (HPCI) Out-of-Service; and*'B' Emergency Service Water (ESW) with 'A' ESW Out-of-Service.


{{a|1R23}}
====b. Findings====
==1R23 Temporary Plant Modifications.......................................7==
No findings of significance were identified..2Complete System Walkdown (71111.04S - 1 Sample)


1EP2Alert and Notification System (ANS) Evaluation..........................71EP3Emergency Response Organization (ERO) Staffing and Augmentation System.8 1EP4Emergency Action Level (EAL) and Emergency Plan Changes..............81EP5Correction of Emergency Preparedness Weaknesses.....................91EP6Drill Evaluation...................................................9RADIATION SAFETY........................................................102PS2Radioactive Material Processing and Transportation.....................10OTHER ACTIVITIES.........................................................134OA1Performance Indicator (PI) Verification...............................134OA2Identification and Resolution of Problems.............................144OA3Event Followup.................................................16 4OA5Other Activities..................................................23 4OA6Meetings, Including Exit...........................................23 4OA7Licensee-Identified Violations......................................23
====a. Inspection Scope====
During the week of June 25, 2007, the inspectors performed one complete Unit 2 highpressure service water (HPSW) system walkdown of the accessible portions of the 3Enclosuresystem. The full walkdown was performed to identify any discrepancies which couldimpact the Unit 2 HPSW system function. The inspectors reviewed system operating procedures, piping and instrumentation drawings, walked down control system components, and verified that circuit breakers and valves were in the appropriate positions.


=SUPPLEMENTAL INFORMATION=
====b. Findings====
No findings of significance were identified.
{{a|1R05}}
==1R05 Fire Protection (71111.05Q - 10 Samples)Fire Protection - Tours==


==KEY POINTS OF CONTACT==
====a. Inspection Scope====
.................................................A-1
The inspectors reviewed PBAPS's Fire Protection Plan, Technical Requirements Manual(TRM), and the respective pre-fire action plan procedures to determine the required fire protection design features, fire area boundaries, and combustible loading requirements for the areas examined during this inspection. The fire risk analysis was reviewed to gain risk insights regarding the areas selected for inspection. The inspectors performed walkdowns of ten areas to assess the material condition of active and passive fire protection systems and features. The inspection was also performed to verify the adequacy of the control of transient combustible material and ignition sources, the condition of manual firefighting equipment, fire barriers, and the status of any related compensatory measures. The following ten fire areas were reviewed for impaired fire protection features:*Unit 3 Reactor Building (RB), RCIC Room, 88' Elevation (Fire Zone 63);*Standby Gas Treatment Room, Radwaste Building, 91'6" Elevation (Fire Zone 70);
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
*Unit 3 RB, North Control Rod Drive (CRD) Equipment and West Corridor (Fire Zone 13H);*Unit 3 Refuel Floor (Fire Zone 55);
............................A-1
==LIST OF DOCUMENTS REVIEWED==
...........................................A-2
==LIST OF ACRONYMS==
......................................................A-10
: [[SUMMAR]] [[Y]]
: [[OF]] [[]]
: [[FINDIN]] [[]]
GSIR 05000277/2007-003, 05000278/2007-003; 04/01/2007 - 06/30/2007; Peach Bottom AtomicPower Station (PBAPS), Units 2 and 3; Event Followup. The report covered a 3-month period of inspection by resident inspectors, a senior projectengineer, and announced inspections by a senior health physicist, a senior emergency response
coordinator, and an emergency preparedness inspector. Three Green findings, two of which
were NCVs, were identified. The significance of most findings is indicated by their color (Green,
White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination
Process" (SDP). Findings for which the SDP does not apply may be Green or be assigned a
severity level after
: [[NRC]] [[management review. The]]
NRC's program for overseeing the safe
operation of commercial nuclear power reactors is described in
: [[NUR]] [[]]
EG-1649, "Reactor Oversight
Process," Revision 4, dated December 2006.
: [[A.NRC]] [[-Identified and Self-Revealing FindingsCornerstone:  Mitigating Systems*Green. A self-revealing finding was identified for inadequate implementation ofwork order (]]
WO) instructions to verify the correct breaker frame size during the
overhaul of a compatible spare breaker for installation into the '4T4' 480 volt load
center. This condition resulted in a poor electrical connection between the primary
disconnect fingers and the switchgear bus stabs for one breaker in the '4T4' load
center that ultimately resulted in a fire that led to a plant transient and declaration
of an Unusual Event (UE).This finding is greater than minor because it affected the human performanceattribute of the Initiating Event Cornerstone, in that, an incorrect frame size
breaker was installed into a cubicle for which it was not sized. This mismatch
caused an electrical fault that led to a fire and a plant transient that upset plant
stability. The finding was of very low safety significance (Green) because it did not
increase both the likelihood of a reactor scram and that mitigation equipment or
functions would not be available. The inspectors determined that this finding had a
cross-cutting aspect in the area of human performance (work practices
component) because maintenance technicians did not follow  WO instructions to
specifically verify the frame size of a breaker during its overhaul  (IMC 0305 aspect
: [[H.]] [[4(b)).  (Section 4]]
: [[OA]] [[3.1)*Green. A self-revealing]]
: [[NCV]] [[of Technical Specification (]]
TS) 5.4.1, was identifiedwhen operators inadequately implemented a surveillance test by missing a
procedure step. The missed step placed the E-3 emergency diesel generator
(EDG) in the isochronous mode of operation while it was synchronized to off-site
power and resulted in an unexpected over-loading of the E-3 EDG. This finding is more than minor because it was associated with the humanperformance attribute of the Mitigating Systems Cornerstone, and impacted the
cornerstone objective of ensuring the availability of the E-3 EDG to respond to
initiating events. This finding is of very low safety significance (Green) because all
other
: [[EDG]] [[s remained operable and the actual loss of safety function of the E-3]]
: [[EDG]] [[was less than the]]
TS allowed outage time of seven days. The inspectors
ivdetermined that this finding had a cross-cutting aspect in the area of humanperformance (work practices component) because
: [[PBA]] [[]]
PS personnel did not follow
procedures when the E-3 EDG was placed in the isochronous load control mode
with the E-3
: [[EDG]] [[in parallel with the off-site power source (]]
: [[IMC]] [[0305 aspect]]
: [[H.]] [[4(b)).  (Section 4]]
: [[OA]] [[3.2)*Green. A self-revealing]]
: [[NCV]] [[of]]
TS 5.4.1, was identified when operatorsmanipulated a diesel-driven fire pump (DDFP) cooling water valve outside of
procedure guidance. The improper manipulation led to misalignment of the
: [[DD]] [[]]
FP
cooling water that subsequently damaged the engine during operations without
cooling water. The failure to use a procedure for cleaning and restoring the
: [[DD]] [[]]
FP cooling waterstrainer was a more than minor finding because it was associated with the
degradation of a fire protection feature, in that, the
: [[DD]] [[]]
FP was rendered inoperable
by damage to the engine. Using the Fire Protection SDP, the finding was
determined to be of very low safety significance due to the motor-driven fire pump
remaining operable during the five days the
: [[DD]] [[]]
FP was inoperable, and the small
number of fire scenarios which would impact the power supply to the motor-driven
fire pump. This finding had a cross-cutting aspect in the area of human
performance (resources component) because procedure ST-O-37D-340-2 did not
provide complete and accurate instructions for cleaning the
: [[DD]] [[]]
FP cooling water
strainer (IMC 0305 aspect
: [[H.]] [[2©).  (Section 4]]
OA3.3)B.Licensee-Identified Violations Three violations of very low safety significance (Green), that were identified by thelicensee, have been reviewed by the inspectors. Corrective actions taken or planned by
the licensee have been entered into the licensee's CAP. The violations and corrective
actions are listed in Section 4OA7 of this report.
EnclosureREPORT
: [[DETAIL]] [[]]
SSummary of Plant StatusUnit 2 began the inspection period at 100 percent full rated thermal power (RTP) until April 27, 2007, when power was reduced to 58 percent for planned waterbox cleaning, control
rod testing, 2 'A' reactor feed pump (RFP) maintenance, and other planned maintenance
and testing. On April 28, 2007, the unit returned to full power where it remained until the end of
the inspection period, except for brief periods to support planned testing and rod pattern
adjustments. Unit 3 began the inspection period at 100 percent full RTP until April 16, 2007, when anunplanned power reduction to 84 percent was performed in response to rapidly increasing
'A' reactor recirculation pump shaft seal temperatures. The unit returned to full power on
April 18, 2007. On May 4, 2007, power was reduced to 59 percent for planned waterbox
cleaning, control rod testing, and 3 'C' RFP maintenance. The unit returned to full power on
May 5, 2007. On May 11, 2007, power was reduced to 65 percent for a planned control rod
pattern adjustment and RFP testing, and the unit returned to full power on May 12, 2007. On
June 15, 2007, power was reduced to 82 percent for a rod pattern adjustment and planned
maintenance on a feedwater heater drain line. The unit was returned to full power on June 16,
2007, where it remained until the end of the inspection period, except for brief periods to support
planned testing and rod pattern adjustments.
: [[1.REACT]] [[]]
: [[OR]] [[]]
: [[SAFET]] [[]]
YCornerstones:  Initiating Events, Mitigating Systems, and Barrier Integrity1R01Adverse Weather Protection (71111.01 - 1 System Sample; 1 Site Sample).1Summer Seasonal Readiness    a.Inspection ScopeThe inspectors performed one seasonal readiness sample that included a review of threeventilation systems. Specifically, the inspectors reviewed the procedures listed in
to the report, and verified summer ventilation system alignment for the
diesel generator building, circulating water pump structure, and circulating water pump
screen house. b.FindingsNo findings of significance were identified.
2Enclosure.2Adverse Weather Event Review    a.Inspection ScopeOn June 13, 2007, a tornado warning was issued for an adjacent county. The inspectorsreviewed
: [[PBA]] [[]]
PS's actions taken to respond to potential adverse environmental conditions
from severe thunderstorms that entered the area. High winds, lightning, rain, and reports
of hail were experienced at the site. The inspectors observed that
: [[PBA]] [[]]
PS's personnel
consulted procedure
: [[OP]] [[-]]
PB-108-111-1001, "Preparation for Severe Weather," increased
the online risk assessment to "Yellow," and subsequently implemented procedure
AO 53.2-0, "Equipment Checks After a Thunderstorm."  b.FindingsNo findings of significance were identified.1R04Equipment Alignment (71111.04Q - 3 Partial Walkdown Samples).1Partial Walkdown  a.Inspection ScopeThe inspectors performed a partial walkdown of three systems to verify the operability ofredundant or diverse trains and components when safety-related equipment was
inoperable. The inspectors performed walkdowns to identify any discrepancies that could
impact the function of the system and potentially increase risk. The inspectors reviewed
applicable operating procedures, walked down system components, and verified that
selected breakers, valves, and support equipment were in the correct position to support
system operation. The inspectors also verified that
: [[PBA]] [[]]
PS had properly identified and
resolved equipment alignment problems that could cause initiating events or impact the
capability of mitigating systems or barriers and entered them into the CAP. The three
systems reviewed were: *E-3 Diesel Generator and 3 Startup Transformer with the 2 Startup TransformerOut-of-Service;*Unit 2 Reactor Core Isolation Cooling (RCIC) with Unit 2 High Pressure CoolantInjection (HPCI) Out-of-Service; and*'B' Emergency Service Water (ESW) with 'A'
: [[ESW]] [[Out-of-Service. b.FindingsNo findings of significance were identified..2Complete System Walkdown (71111.04S - 1 Sample)  a.Inspection ScopeDuring the week of June 25, 2007, the inspectors performed one complete Unit 2 highpressure service water (]]
HPSW) system walkdown of the accessible portions of the
3Enclosuresystem. The full walkdown was performed to identify any discrepancies which couldimpact the Unit
: [[2 HP]] [[]]
SW system function. The inspectors reviewed system operating
procedures, piping and instrumentation drawings, walked down control system
components, and verified that circuit breakers and valves were in the appropriate
positions. b.FindingsNo findings of significance were identified.1R05Fire Protection (71111.05Q - 10 Samples)Fire Protection - Tours  a.Inspection ScopeThe inspectors reviewed
: [[PBAPS]] [['s Fire Protection Plan, Technical Requirements Manual(]]
TRM), and the respective pre-fire action plan procedures to determine the required fire
protection design features, fire area boundaries, and combustible loading requirements for
the areas examined during this inspection. The fire risk analysis was reviewed to gain risk
insights regarding the areas selected for inspection. The inspectors performed
walkdowns of ten areas to assess the material condition of active and passive fire
protection systems and features. The inspection was also performed to verify the
adequacy of the control of transient combustible material and ignition sources, the
condition of manual firefighting equipment, fire barriers, and the status of any related
compensatory measures. The following ten fire areas were reviewed for impaired fire
protection features:*Unit 3 Reactor Building (RB),
: [[RC]] [[]]
IC Room, 88' Elevation (Fire Zone 63);*Standby Gas Treatment Room, Radwaste Building, 91'6" Elevation (Fire Zone 70);
*Unit
: [[3 RB]] [[, North Control Rod Drive (]]
CRD) Equipment and West Corridor (Fire Zone 13H);*Unit 3 Refuel Floor (Fire Zone 55);
*Unit 3 'A' and 'C' Core Spray Rooms (Fire Zones 13D & 13E);
*Unit 3 'A' and 'C' Core Spray Rooms (Fire Zones 13D & 13E);
*Unit 2 Emergency Battery/Switchgear Rooms (Fire Zone 127);
*Unit 2 Emergency Battery/Switchgear Rooms (Fire Zone 127);
*Unit
*Unit 2 RCIC (Fire Zone 60);  
: [[2 RC]] [[]]
IC (Fire Zone 60);  
*Unit 2 Main Transformer Yard (Fire Zone 151);
*Unit 2 Main Transformer Yard (Fire Zone 151);
*2 Startup Switchgear Building (Fire Zone 164); and
*2 Startup Switchgear Building (Fire Zone 164); and
*Diesel Generator Building, 127' Elevation (Fire Zone 132). b.FindingsNo findings of significance were identified.
*Diesel Generator Building, 127' Elevation (Fire Zone 132).
4Enclosure1R11Licensed Operator Requalification Program (71111.11Q - 1 Sample) Resident Inspector Quarterly Review a.Inspection ScopeOn June 12, 2006, the inspectors observed operators in
 
: [[PBA]] [[]]
====b. Findings====
PS's simulator duringlicensed operator requalification training to verify that operator performance was adequate
No findings of significance were identified.
and that evaluators were identifying and documenting crew performance issues. The
 
inspectors verified that performance issues were discussed in the crew's post-scenario
4Enclosure1R11Licensed Operator Requalification Program (71111.11Q - 1 Sample) Resident Inspector Quarterly Review
critiques. The inspectors also observed operator implementation of procedures. The
 
inspectors discussed the training, simulator scenarios, and critiques with the operators,
====a. Inspection Scope====
shift supervision, and the training instructors. The evaluated scenario observed for this
On June 12, 2006, the inspectors observed operators in PBAPS's simulator duringlicensed operator requalification training to verify that operator performance was adequate and that evaluators were identifying and documenting crew performance issues. The inspectors verified that performance issues were discussed in the crew's post-scenario critiques. The inspectors also observed operator implementation of procedures. The inspectors discussed the training, simulator scenarios, and critiques with the operators, shift supervision, and the training instructors. The evaluated scenario observed for this one sample involved the events listed below: *Small Break Loss of Coolant Accident; and*An Anticipated Transient Without Scram.
one sample involved the events listed below: *Small Break Loss of Coolant Accident; and*An Anticipated Transient Without Scram. b.FindingsNo findings of significance were identified.1R12Maintenance Effectiveness (71111.12Q - 2 Samples) a.Inspection ScopeThe inspectors reviewed two samples of
 
: [[PBAPS]] [['s evaluation of degraded conditionsinvolving safety-related structures, systems, and components (]]
====b. Findings====
SSCs) for maintenance
No findings of significance were identified.
effectiveness during this inspection period. The inspectors reviewed
{{a|1R12}}
: [[PBA]] [[]]
==1R12 Maintenance Effectiveness (71111.12Q - 2 Samples)==
PS's
 
implementation of the Maintenance Rule (MR), and verified that the conditions associated
====a. Inspection Scope====
with the referenced condition reports (CRs) were evaluated against applicable MR
The inspectors reviewed two samples of PBAPS's evaluation of degraded conditionsinvolving safety-related structures, systems, and components (SSCs) for maintenance effectiveness during this inspection period. The inspectors reviewed PBAPS's implementation of the Maintenance Rule (MR), and verified that the conditions associated with the referenced condition reports (CRs) were evaluated against applicable MR functional failure criteria as found in the licensee's scoping documents and procedures.
functional failure criteria as found in the licensee's scoping documents and procedures.
 
The inspectors also discussed these issues with system engineers and MR coordinators
The inspectors also discussed these issues with system engineers and MR coordinators to verify that they were tracked against performance criteria and that the systems were classified in accordance with MR implementation guidance. Documents reviewed during the inspection are listed in the Attachment. The following conditions were reviewed:*Issue Report (IR) 587171, ESW Check Valve (CHK-0-33-515A) - Not SeatedCauses ESW ST-O-033-300-2 to be Aborted; and*IR 622560, Maintenance Preventable Functional Failure for Loss of '4T4' 480 VoltLoad Center.
to verify that they were tracked against performance criteria and that the systems were
 
classified in accordance with MR implementation guidance. Documents reviewed during
====b. Findings====
the inspection are listed in the Attachment. The following conditions were reviewed:*Issue Report (IR) 587171,
No findings of significance were identified.
: [[ESW]] [[Check Valve (]]
 
: [[CHK]] [[-0-33-515A) - Not SeatedCauses]]
5Enclosure1R13Maintenance Risk Assessments and Emergent Work Control (71111.13 - 8 Samples)
: [[ESW]] [[]]
 
ST-O-033-300-2 to be Aborted; and*IR 622560, Maintenance Preventable Functional Failure for Loss of '4T4' 480 VoltLoad Center. b.FindingsNo findings of significance were identified.
====a. Inspection Scope====
5Enclosure1R13Maintenance Risk Assessments and Emergent Work Control (71111.13 - 8 Samples) a.Inspection ScopeThe inspectors evaluated
The inspectors evaluated PBAPS's implementation of their maintenance risk program toverify that PBAPS managed risk in accordance with 10 CFR Part 50.65(a)(4). Procedure WC-AA-101, "On-line Work Control Process," was also reviewed. This inspection included reviews of PBAPS's use of the Paragon online risk monitoring software. The inspectors reviewed equipment tracking documentation, daily work schedules, and performed plant tours. The following activities selected were based on plant maintenance schedules and systems that contributed to risk. The inspectors completed eight evaluations of maintenance activities on the following:*Troubleshooting, Rework and Testing (TRT) Control Form No. 07-18, Monitor3 'A' Recirculation Pump Seal Parameters During Recirculation Pump Speed Changes;*TRT No. 07-020, Re-align CRD Pump Suction to the Condensate Storage Tank(CST) from the Condensate System;*WO C0220911, Calibrate, Repair & Replace E-2 EDG Temperature Switch;
: [[PBAPS]] [['s implementation of their maintenance risk program toverify that]]
*WO A1613202, 3 'B' Recirculation Pump 2 nd Stage Seal Pressure;*IR 623723, Bolt and Heli-coil Found Damaged at Disassembly on 00T634;
: [[PBAPS]] [[managed risk in accordance with 10 CFR Part 50.65(a)(4). Procedure]]
: [[WC]] [[-]]
AA-101, "On-line Work Control Process," was also reviewed. This inspection
included reviews of
: [[PBA]] [[]]
PS's use of the Paragon online risk monitoring software. The
inspectors reviewed equipment tracking documentation, daily work schedules, and
performed plant tours. The following activities selected were based on plant maintenance
schedules and systems that contributed to risk. The inspectors completed eight
evaluations of maintenance activities on the following:*Troubleshooting, Rework and Testing (TRT) Control Form No. 07-18, Monitor3 'A' Recirculation Pump Seal Parameters During Recirculation Pump Speed
Changes;*TRT No. 07-020, Re-align
: [[CRD]] [[Pump Suction to the Condensate Storage Tank(]]
CST) from the Condensate System;*WO C0220911, Calibrate, Repair & Replace E-2 EDG Temperature Switch;
*WO A1613202, 3 'B' Recirculation Pump 2nd Stage Seal Pressure;*IR 623723, Bolt and Heli-coil Found Damaged at Disassembly on 00T634;
*IR 626534, Equipment Not Protected As Required;  
*IR 626534, Equipment Not Protected As Required;  
*WO R0736769-01, Core Spray Loop 'A' Full Flow Test Valve Operator,MO-2-14-026A-OP, Perform Motor Operator Preventive Maintenance; and*IR 542109, 2 'C' Service Air Compressor Trip.Additionally, the inspectors verified that an inspector-identified issue,
*WO R0736769-01, Core Spray Loop 'A' Full Flow Test Valve Operator,MO-2-14-026A-OP, Perform Motor Operator Preventive Maintenance; and*IR 542109, 2 'C' Service Air Compressor Trip.Additionally, the inspectors verified that an inspector-identified issue, IR 626534,"Equipment Not Protected As Required," was entered into the PBAPS's CAP.
: [[IR]] [[626534,"Equipment Not Protected As Required," was entered into the]]
 
PBAPS's CAP. b.FindingsNo findings of significance were identified.1R15Operability Evaluations (71111.15 - 5 Samples) a.Inspection ScopeThe inspectors reviewed five issues to assess the technical adequacy of the evaluations,the use and control of compensatory measures, and compliance with the licensing and
====b. Findings====
design bases. Associated adverse condition monitoring plans, engineering technical
No findings of significance were identified.
evaluations, and operational and technical decision making documents were also
{{a|1R15}}
reviewed. The inspectors verified these processes were performed in accordance with
==1R15 Operability Evaluations (71111.15 - 5 Samples)==
the applicable procedures. The inspectors used
 
: [[TS]] [[,]]
====a. Inspection Scope====
TRM, the Updated Final Safety
The inspectors reviewed five issues to assess the technical adequacy of the evaluations,the use and control of compensatory measures, and compliance with the licensing and design bases. Associated adverse condition monitoring plans, engineering technical evaluations, and operational and technical decision making documents were also reviewed. The inspectors verified these processes were performed in accordance with the applicable procedures. The inspectors used TS, TRM, the Updated Final Safety Analysis Report (UFSAR), and associated Design Basis Documents (DBDs) as referencesduring these reviews. The issues reviewed included:*Non-Safety Related Piece Installed in E-4 EDG Part (IR 615413);*Rising 3 'A' Reactor Recirculation Pump (RRP) #2 Seal Temperature (IR 617988);
Analysis Report (UFSAR), and associated Design Basis Documents (DBDs) as referencesduring these reviews. The issues reviewed included:*Non-Safety Related Piece Installed in E-4
*Provide Supplemental Cooling to the 3 'A' RRP Seal (IR 618478);
: [[EDG]] [[Part (]]
6EnclosureTarget Rock Safety/Relief Valve (SRV) Seal Welds:  Potential Code Issue(IR 628251); andSmall Leak on 2 'B' Main Steam Line Differential Pressure Instrument LineSnubber Threaded Cap (IR 627026).
IR 615413);*Rising 3 'A' Reactor Recirculation Pump (RRP) #2 Seal Temperature (IR 617988);
 
*Provide Supplemental Cooling to the 3 'A'
====b. Findings====
: [[RRP]] [[Seal (]]
No findings of significance were identified.
IR 618478);
{{a|1R19}}
6EnclosureTarget Rock Safety/Relief Valve (SRV) Seal Welds:  Potential Code Issue(IR 628251); andSmall Leak on 2 'B' Main Steam Line Differential Pressure Instrument LineSnubber Threaded Cap (IR 627026). b.FindingsNo findings of significance were identified.1R19Post-Maintenance Testing (71111.19 - 7 Samples) a.Inspection ScopeThe inspectors observed selected portions of post-maintenance testing (PMT) activitiesand reviewed completed test records. The inspectors observed whether the tests were
==1R19 Post-Maintenance Testing (71111.19 - 7 Samples)==
performed in accordance with the approved procedures and assessed the adequacy of
 
the test methodology based on the scope of maintenance work performed. In addition,
====a. Inspection Scope====
the inspectors assessed the test acceptance criteria to evaluate whether the test
The inspectors observed selected portions of post-maintenance testing (PMT) activitiesand reviewed completed test records. The inspectors observed whether the tests were performed in accordance with the approved procedures and assessed the adequacy of the test methodology based on the scope of maintenance work performed. In addition, the inspectors assessed the test acceptance criteria to evaluate whether the test demonstrated that the tested components satisfied the applicable design and licensing bases and the TS requirements. The inspectors reviewed the recorded test data to verify that the acceptance criteria were satisfied. The inspectors reviewed seven PMTs performed in conjunction with the following maintenance activities:*WO C0220911, Calibrate, Repair & Replace E-2 EDG Temperature Switch;*WO R1049367, Unit 3 Hydraulic Control Unit (HCU) 50-43: HCU Overhaul;
demonstrated that the tested components satisfied the applicable design and licensing
*WO R1017055, DDFP (00P063-DR) Diesel Engine 6YR Overhaul;
bases and the TS requirements. The inspectors reviewed the recorded test data to verify
*WO C0216504, RCIC Suction Pressure Switch (PS-2-13-067-01), Replace Pressure Switch; WO C0221445, Inspect/Repair/Replace Unit 2 'C' Main Steam Line Radiation Monitor (RIS-2-17-251C);*WO C0215740, Replace Unit 2 'B' Reactor Protection System Motor Generator Set Endbell; and*WO R0629147, Perform Motor Control Unit Inspection on the 'C' Glycol Pump.
that the acceptance criteria were satisfied. The inspectors reviewed seven PMTs
 
performed in conjunction with the following maintenance activities:*WO C0220911, Calibrate, Repair & Replace E-2
====b. Findings====
: [[EDG]] [[Temperature Switch;*]]
No findings of significance were identified.
WO R1049367, Unit 3 Hydraulic Control Unit (HCU) 50-43: HCU Overhaul;
{{a|1R22}}
*WO R1017055,
==1R22 Surveillance Testing (71111.22 - 5 Samples) [3 Routine Samples; 1 IST Sample; 1Reactor Coolant System (RCS) Leakage Sample]==
: [[DDFP]] [[(00P063-]]
 
DR) Diesel Engine 6YR Overhaul;
====a. Inspection Scope====
*WO C0216504,
The inspectors reviewed and observed portions of selected surveillance tests (STs), andcompared test data with established acceptance criteria to verify the systems demonstrated the capability of performing the intended safety functions. The inspectors also verified that the systems and components maintained operational readiness, met applicable TS requirements, and were capable of performing the design basis functions.
: [[RCIC]] [[Suction Pressure Switch (]]
 
PS-2-13-067-01), Replace Pressure Switch;
WO C0221445, Inspect/Repair/Replace Unit 2 'C' Main Steam Line Radiation
Monitor (RIS-2-17-251C);*WO C0215740, Replace Unit 2 'B' Reactor Protection System Motor Generator Set Endbell; and*WO R0629147, Perform Motor Control Unit Inspection on the 'C' Glycol Pump. b.FindingsNo findings of significance were identified.1R22Surveillance Testing (71111.22 - 5 Samples) [3 Routine Samples;
: [[1 IST]] [[Sample; 1Reactor Coolant System (]]
RCS) Leakage Sample] a.Inspection ScopeThe inspectors reviewed and observed portions of selected surveillance tests (STs), andcompared test data with established acceptance criteria to verify the systems
demonstrated the capability of performing the intended safety functions. The inspectors
also verified that the systems and components maintained operational readiness, met
applicable TS requirements, and were capable of performing the design basis functions.
The five STs reviewed and observed included:
The five STs reviewed and observed included:
7Enclosure*ST-O-023-301-3,
7Enclosure*ST-O-023-301-3, HPCI Pump, Valve, Flow and Unit Cooler Functional andIn-Service Test  [IST Sample];*ST-O-020-560-2 & 3, Reactor Coolant Leakage Test [RCS Leakage Sample];
: [[HPCI]] [[Pump, Valve, Flow and Unit Cooler Functional andIn-Service Test  []]
IST Sample];*ST-O-020-560-2 & 3, Reactor Coolant Leakage Test [RCS Leakage Sample];
*ST-I-60A-230-3, Linear Power Range Monitor Gain Calibration;
*ST-I-60A-230-3, Linear Power Range Monitor Gain Calibration;
*SI2T-MIS-8547-C1CQ, Calibration/Functional Check of Channel 'C' Group 1, 4and 5 of Primary Containment Isolation Valve (PCIV) Logic for
*SI2T-MIS-8547-C1CQ, Calibration/Functional Check of Channel 'C' Group 1, 4and 5 of Primary Containment Isolation Valve (PCIV) Logic for TSs-80547C; and*ST-R-003-485-3, CRD Scram Insertion Timing of Selected Control Rods.b.FindingsNo findings of significance were identified.
: [[TS]] [[s-80547C; and*]]
{{a|1R23}}
ST-R-003-485-3, CRD Scram Insertion Timing of Selected Control Rods.b.FindingsNo findings of significance were identified.1R23Temporary Plant Modifications (71111.23 -1 Sample) a.Inspection ScopeThe inspectors reviewed one temporary modification to verify that implementation of themodification did not place the plant in an unsafe condition. The review was also
==1R23 Temporary Plant Modifications (71111.23 -1 Sample)==
conducted to verify that the design bases, licensing bases, and performance capability ofrisk significant SSCs had not been degraded as a result of the modification. The
 
inspectors verified the modified equipment alignment through control room
====a. Inspection Scope====
instrumentation observations; the
The inspectors reviewed one temporary modification to verify that implementation of themodification did not place the plant in an unsafe condition. The review was also conducted to verify that the design bases, licensing bases, and performance capability ofrisk significant SSCs had not been degraded as a result of the modification. The inspectors verified the modified equipment alignment through control room instrumentation observations; the UFSAR; drawings; procedures; WO reviews; and plant walkdowns of accessible equipment. The following temporary modification was reviewed:*TCCP 07-00172, Install Cooling Unit to Assist 3 'A' RRP Seal Cooling.
: [[UFSAR]] [[; drawings; procedures;]]
 
WO reviews; and plant
====b. Findings====
walkdowns of accessible equipment. The following temporary modification was reviewed:*TCCP 07-00172, Install Cooling Unit to Assist 3 'A'
No findings of significance were identified.Cornerstone: Emergency Preparedness1EP2Alert and Notification System (ANS) Evaluation (71114.02 - 1 Sample)
: [[RRP]] [[Seal Cooling. b.FindingsNo findings of significance were identified.Cornerstone: Emergency Preparedness1]]
 
: [[EP]] [[2Alert and Notification System (ANS) Evaluation (71114.02 - 1 Sample) a.Inspection Scope An onsite review was conducted to assess the maintenance and testing of the]]
====a. Inspection Scope====
: [[PBAPS]] [['s]]
An onsite review was conducted to assess the maintenance and testing of the PBAPS'sANS. During this inspection, the inspectors interviewed emergency preparedness (EP)staff responsible for implementation of the ANS testing and maintenance. IRs pertaining to the ANS were reviewed for causes, trends, and corrective actions. The inspectors further discussed with PBAPS, the ANS siren system and its performance from July 2005 through May 2007. The inspectors reviewed the licensee's procedures and the ANS design report to ensure compliance with those commitments for system maintenance and testing. The inspection was conducted in accordance with NRC Inspection Procedure (IP)71114, Attachment 2. Planning standard, 10 CFR 50.47(b)(5) and the related requirements of 10 CFR 50, Appendix E were used as reference criteria.
ANS. During this inspection, the inspectors interviewed emergency preparedness (EP)
 
staff responsible for implementation of the
====b. Findings====
: [[ANS]] [[testing and maintenance.]]
No findings of significance were identified.1EP3Emergency Response Organization (ERO) Staffing and Augmentation System (71114.03 - 1 Sample)
IRs pertaining
 
to the ANS were reviewed for causes, trends, and corrective actions. The inspectors
====a. Inspection Scope====
further discussed with
A review of Peach Bottom's ERO augmentation staffing requirements and the process fornotifying the ERO was conducted. This was performed to ensure the readiness of key staff for responding to an event and to ensure timely facility activation. The inspectors reviewed procedures and IRs associated with the ERO notification system and drills, and reviewed records from call-in drills. The inspectors interviewed personnel responsible for testing the ERO augmentation process, and reviewed the training records for a sampling of the ERO to ensure training and qualifications were up-to-date. The inspectors reviewed procedures for ERO administration and training, and verified a sampling of the ERO participated in exercises in 2005 and 2006. The inspectors also reviewed records of offsite agency training and the June 2007 Respirator Qualification Report. The inspection was conducted in accordance with NRC IP 71114, Attachment 3. Planning standard, 10 CFR 50.47(b)(2) and related requirements of 10 CFR 50, Appendix E were used as reference criteria.
: [[PBAPS]] [[, the]]
 
ANS siren system and its performance from July 2005
====b. Findings====
through May 2007. The inspectors reviewed the licensee's procedures and the ANS
No findings of significance were identified. 1EP4Emergency Action Level (EAL) and Emergency Plan Changes (71114.04 - 1 Sample)
design report to ensure compliance with those commitments for system maintenance and
 
testing. The inspection was conducted in accordance with
====a. Inspection Scope====
: [[NRC]] [[Inspection Procedure (]]
Since the last NRC inspection of this program area, Emergency Plan (Plan), Revision 26,was implemented based on PBAPS's determination, in accordance with 10 CFR 50.54(q), that the changes resulted in no decrease in effectiveness of the Plan, and that the revised Plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR 50. The inspectors conducted a sampling review of the Emergency Plan changes, and changes to the lower-tier Emergency Plan implementing procedures, to evaluate the changes for potential decreases in effectiveness of the Emergency Plan. However, this review was not documented in a safety evaluation report and does not constitute formal NRC approval of the changes. Therefore, these changes remain subject to future NRC inspection in their entirety.
IP)
 
71114, Attachment 2. Planning standard, 10 CFR 50.47(b)(5) and the related
====b. Findings====
requirements of 10 CFR 50, Appendix E were used as reference criteria.
No findings of significance were identified.
8Enclosure    b.FindingsNo findings of significance were identified.1EP3Emergency Response Organization (ERO) Staffing and Augmentation System (71114.03 - 1 Sample)
 
a.Inspection Scope A review of Peach Bottom's
9Enclosure1EP5Correction of Emergency Preparedness Weaknesses (71114.05 - 1 Sample)
: [[ERO]] [[augmentation staffing requirements and the process fornotifying the]]
 
ERO was conducted. This was performed to ensure the readiness of key
====a. Inspection Scope====
staff for responding to an event and to ensure timely facility activation. The inspectors
The inspectors reviewed a sampling of self-assessment procedures and reports to assessPBAPS's ability to evaluate their performance and programs. The inspectors reviewed a sampling of IRs from July 2006 through May 2007, initiated by Exelon Nuclear at Peach Bottom from drills, self-assessments, and audits. Other drill reports reviewed included:
reviewed procedures and
medical/health physics, fire, integrated, and call-in.
: [[IR]] [[s associated with the]]
 
ERO notification system and drills, and
Additionally, the inspectors reviewed the three UE Evaluation Reports generated since the last inspection, and audits for 2006 and 2007 required by 50.54(t). This inspection was conducted in accordance with NRC IP 71114, Attachment 5. Planning standard, 10 CFR 50.47(b)(14) and the related requirements of 10 CFR 50, Appendix E were used as reference criteria.
reviewed records from call-in drills. The inspectors interviewed personnel responsible for
 
testing the ERO augmentation process, and reviewed the training records for a sampling
====b. Findings====
of the ERO to ensure training and qualifications were up-to-date. The inspectors reviewed
No findings of significance were identified.1EP6Drill Evaluation (71114.06 - 1 Sample)Off-Year Exercise (Drill)
procedures for
 
: [[ERO]] [[administration and training, and verified a sampling of the]]
====a. Inspection Scope====
ERO
The inspectors conducted this inspection to assess:  training quality and conduct;emergency plan procedure implementation; facility and equipment readiness; personnel performance in drills and exercises; organizational and management changes; and communications equipment readiness. The primary focus of this inspection was to verify PBAPS's critique of classification, notification, and protective action recommendation (PAR) development.On May 15, 2007, the inspectors observed a full scale drill. The primary focus of thisinspection was to verify PBAPS's critique of classification, notification, and PAR development. Selected portions of the drill were observed in the control room simulator and later in the technical support center (TSC). The drill scenario began with a simulated internal flooding event in the 2 'A' residual heat removal (RHR) pump room that degraded the performance of the associated safety system. The drill scenario continued with a simulated reactor event that started with a reduction of coolant flow to the core and progressed until three fission product barriers (fuel cladding, RCS, and containment) were lost.
participated in exercises in 2005 and 2006. The inspectors also reviewed records of
 
offsite agency training and the June 2007 Respirator Qualification Report. The inspection
The inspectors observed licensed operator and ERO personnel adherence to the Emergency Plan implementing procedures. The ERO personnel responses to simulated degraded plant conditions were inspected to identify weaknesses and deficiencies in classification and notification. The inspectors also observed the transition of responsibility for the ERO from the shift manager in the simulated control room to the TSC. The inspectors observed PBAPS's critique of the drill to evaluate PBAPS's identification of weaknesses and deficiencies. The inspectors compared PBAPS's identified issues against the inspectors' observations to determine whether PBAPS adequately identified problems and entered them into the CAP. This inspection activity represented one 10Enclosuresample. The documents and procedures reviewed during the inspection are listed in theAttachment.
was conducted in accordance with
 
: [[NRC]] [[]]
====b. Findings====
: [[IP]] [[71114, Attachment 3. Planning standard,]]
No findings of significance were identified.2.RADIATION SAFETYCornerstone:  Public Radiation Safety 2PS2Radioactive Material Processing and Transportation (71122.02 - 5 Samples).1Inspection Planning/In-Office Inspection
: [[CFR]] [[50.47(b)(2) and related requirements of 10]]
 
CFR 50, Appendix E were used as
====a. Inspection Scope====
reference criteria. b.FindingsNo findings of significance were identified.
The inspectors reviewed the solid waste system description in the UFSAR and recentradiological effluent release reports for information on the types and amounts of radioactive waste. The inspectors reviewed Exelon's audit program in the area of radioactive wastecharacterization, transportation, and disposal. The inspectors also reviewed the status of the NRC approved quality assurance program in this area.  (Section 2PS2.6)
: [[1EP]] [[4Emergency Action Level (]]
 
: [[EAL]] [[) and Emergency Plan Changes (71114.04 - 1 Sample) a.Inspection Scope Since the last]]
====b. Findings====
: [[NRC]] [[inspection of this program area, Emergency Plan (Plan), Revision 26,was implemented based on]]
No findings of significance were identified.
PBAPS's determination, in accordance with
 
CFR 50.54(q), that the changes resulted in no decrease in effectiveness of the Plan,
===.2 Radioactive Waste System Walkdown===
and that the revised Plan continued to meet the requirements of 10 CFR 50.47(b) and
 
Appendix E to 10 CFR 50. The inspectors conducted a sampling review of the
====a. Inspection Scope====
Emergency Plan changes, and changes to the lower-tier Emergency Plan implementing
The inspectors walked down accessible portions of the station's radioactive liquid andsolid waste collection, processing, and storage systems and locations to determine if:
procedures, to evaluate the changes for potential decreases in effectiveness of the
systems and facilities were consistent with descriptions provided in the UFSAR; to evaluate their general material conditions; and to identify changes made to systems.
Emergency Plan. However, this review was not documented in a safety evaluation report
 
and does not constitute formal NRC approval of the changes. Therefore, these changes
Areas visually inspected included tank and pump rooms, the de-watering facility, in-plant and outside waste storage areas, outside tank areas, and the low level-waste storage facility. Visual inspection records and previous surveys were also reviewed. The inspector also discussed operation of the radwaste systems with cognizant licensee personnel.The inspectors reviewed the status of any non-operational or abandoned radioactivewaste process equipment; the adequacy of administrative and physical controls for those systems; changes made to radioactive waste processing systems and potential radiological impact, including conduct of safety evaluations of the changes, as necessary.
remain subject to future NRC inspection in their entirety. b.FindingsNo findings of significance were identified.
 
9Enclosure1EP5Correction of Emergency Preparedness Weaknesses (71114.05 - 1 Sample) a.Inspection Scope The inspectors reviewed a sampling of self-assessment procedures and reports to assessPBAPS's ability to evaluate their performance and programs. The inspectors reviewed a
11EnclosureThe inspectors reviewed the current processes for transferring radioactive waste resin andsludge to shipping containers and mixing and sampling of the waste, as appropriate, to evaluate waste mixing, adequacy of sampling, and the methodology for waste concentration averaging. The inspector also reviewed radioactive waste and material storage and handling practices; sources of radioactive waste at the station (waste streams) and processing (as appropriate) and handling of the waste; and the general condition of facilities and equipment. The review was against criteria contained in the station's UFSAR, 10 CFR Part 20,10 CFR 61, the Process Control Program (PCP), and applicable station procedures.
sampling of IRs from July 2006 through May 2007, initiated by Exelon Nuclear at Peach
 
Bottom from drills, self-assessments, and audits. Other drill reports reviewed included:
====b. Findings====
medical/health physics, fire, integrated, and call-in. Additionally, the inspectors reviewed
No findings of significance were identified..3Waste Characterization and Classification
the three UE Evaluation Reports generated since the last inspection, and audits for 2006
 
and 2007 required by 50.54(t). This inspection was conducted in accordance with
====a. Inspection Scope====
: [[NRC]] [[]]
The inspector reviewed the following matters:
IP
71114, Attachment 5. Planning standard, 10 CFR 50.47(b)(14) and the related
requirements of
: [[10 CFR]] [[50, Appendix E were used as reference criteria. b.FindingsNo findings of significance were identified.1]]
EP6Drill Evaluation (71114.06 - 1 Sample)Off-Year Exercise (Drill) a.Inspection ScopeThe inspectors conducted this inspection to assess:  training quality and conduct;emergency plan procedure implementation; facility and equipment readiness; personnel
performance in drills and exercises; organizational and management changes; and
communications equipment readiness. The primary focus of this inspection was to verify
: [[PBA]] [[]]
PS's critique of classification, notification, and protective action recommendation
(PAR) development.On May 15, 2007, the inspectors observed a full scale drill. The primary focus of thisinspection was to verify
: [[PBAPS]] [['s critique of classification, notification, and]]
PAR
development. Selected portions of the drill were observed in the control room simulator
and later in the technical support center (TSC). The drill scenario began with a simulated
internal flooding event in the 2 'A' residual heat removal (RHR) pump room that degraded
the performance of the associated safety system. The drill scenario continued with a
simulated reactor event that started with a reduction of coolant flow to the core and
progressed until three fission product barriers (fuel cladding, RCS, and containment) were
lost. The inspectors observed licensed operator and ERO personnel adherence to the
Emergency Plan implementing procedures. The ERO personnel responses to simulated
degraded plant conditions were inspected to identify weaknesses and deficiencies in
classification and notification. The inspectors also observed the transition of responsibility
for the
: [[ERO]] [[from the shift manager in the simulated control room to the]]
TSC. The
inspectors observed
: [[PBAPS]] [['s critique of the drill to evaluate]]
PBAPS's identification of
weaknesses and deficiencies. The inspectors compared
: [[PBA]] [[]]
PS's identified issues
against the inspectors' observations to determine whether
: [[PBA]] [[]]
PS adequately identified
problems and entered them into the CAP. This inspection activity represented one
10Enclosuresample. The documents and procedures reviewed during the inspection are listed in theAttachment. b.FindingsNo findings of significance were identified.2.RADIATION
: [[SAFETY]] [[Cornerstone:  Public Radiation Safety 2]]
: [[PS]] [[2Radioactive Material Processing and Transportation (71122.02 - 5 Samples).1Inspection Planning/In-Office Inspection a.Inspection ScopeThe inspectors reviewed the solid waste system description in the]]
: [[UFS]] [[]]
AR and recentradiological effluent release reports for information on the types and amounts of
radioactive waste. The inspectors reviewed Exelon's audit program in the area of radioactive wastecharacterization, transportation, and disposal. The inspectors also reviewed the status of
the
: [[NRC]] [[approved quality assurance program in this area.  (Section 2]]
PS2.6) b.FindingsNo findings of significance were identified. .2Radioactive Waste System Walkdown a.Inspection ScopeThe inspectors walked down accessible portions of the station's radioactive liquid andsolid waste collection, processing, and storage systems and locations to determine if:
systems and facilities were consistent with descriptions provided in the
: [[UFS]] [[]]
AR; to
evaluate their general material conditions; and to identify changes made to systems.
Areas visually inspected included tank and pump rooms, the de-watering facility, in-plant
and outside waste storage areas, outside tank areas, and the low level-waste storage
facility. Visual inspection records and previous surveys were also reviewed. The
inspector also discussed operation of the radwaste systems with cognizant licensee
personnel.The inspectors reviewed the status of any non-operational or abandoned radioactivewaste process equipment; the adequacy of administrative and physical controls for those
systems; changes made to radioactive waste processing systems and potential
radiological impact, including conduct of safety evaluations of the changes, as necessary.
11EnclosureThe inspectors reviewed the current processes for transferring radioactive waste resin andsludge to shipping containers and mixing and sampling of the waste, as appropriate, to
evaluate waste mixing, adequacy of sampling, and the methodology for waste
concentration averaging. The inspector also reviewed radioactive waste and material
storage and handling practices; sources of radioactive waste at the station (waste
streams) and processing (as appropriate) and handling of the waste; and the general
condition of facilities and equipment. The review was against criteria contained in the station's
: [[UFSAR]] [[, 10]]
: [[CFR]] [[Part 20,10]]
: [[CFR]] [[61, the Process Control Program (]]
PCP), and applicable station procedures. b.FindingsNo findings of significance were identified..3Waste Characterization and Classification a.Inspection ScopeThe inspector reviewed the following matters:
*Radio-chemical sample analysis results for radioactive waste streams;*Development of scaling factors for difficult to detect and measure radionuclides;
*Radio-chemical sample analysis results for radioactive waste streams;*Development of scaling factors for difficult to detect and measure radionuclides;
*Methods and practices to detect changes in waste streams;  
*Methods and practices to detect changes in waste streams;  
*Classification and characterization of waste relative to
*Classification and characterization of waste relative to 10 CFR 61.55 and 10 CFR 61.56;*Implementation of applicable NRC branch technical positions (BTPs) on wasteclassification, concentration averaging, waste stream determination, and sampling frequency;*Current waste streams and their processing relative to descriptions contained inthe UFSAR and the station's approved PCP; *Current processes for transferring radioactive waste resin and sludge dischargesinto shipping/disposal containers to determine adequacy of sampling;  *Revisions of the PCP and the UFSAR to reflect changes (as appropriate); and
: [[10 CFR]] [[61.55 and 10]]
*Waste processing topical report (de-watering).The inspector discussed the adequacy of samples collected from the waste transfer andde-watering system.The review was against criteria contained in 10 CFR 20, 10 CFR 61, 10 CFR 71, the UFSAR, the PCP, applicable NRC BTPs, and Exelon procedures.
: [[CFR]] [[61.56;*Implementation of applicable]]
 
: [[NRC]] [[branch technical positions (]]
====b. Findings====
BTPs) on wasteclassification, concentration averaging, waste stream determination, and sampling
No findings of significance were identified.
frequency;*Current waste streams and their processing relative to descriptions contained inthe
 
: [[UFSAR]] [[and the station's approved]]
12Enclosure.4Shipment Preparation
: [[PCP]] [[; *Current processes for transferring radioactive waste resin and sludge dischargesinto shipping/disposal containers to determine adequacy of sampling;  *Revisions of the]]
 
: [[PCP]] [[and the]]
====a. Inspection Scope====
UFSAR to reflect changes (as appropriate); and
The inspector observed a non-exempt radioactive material shipment (PM-07-057) inpreparation. The inspector reviewed associated transportation documents, reviewed radiological surveys to support transportation, reviewed license requirements, and discussed preparation with cognizant Exelon personnel. The inspector also reviewed personnel training relative to NRC Bulletin 79-19 and 49 CFR 172, Subpart H. The inspector reviewed and discussed technical training presented to workers. The inspector verified that a training program was provided to personnel responsible for the conduct of radioactive waste processing and radioactive waste shipping activities.
*Waste processing topical report (de-watering).The inspector discussed the adequacy of samples collected from the waste transfer andde-watering system.The review was against criteria contained in
 
: [[10 CFR]] [[20, 10]]
====b. Findings====
: [[CFR]] [[61,]]
No findings of significance were identified.
: [[10 CFR]] [[71, the]]
 
: [[UFSAR]] [[, the]]
===.5 Shipment Records and Documentation===
: [[PCP]] [[, applicable]]
 
NRC BTPs, and Exelon procedures. b.FindingsNo findings of significance were identified.
====a. Inspection Scope====
2Enclosure.4Shipment Preparation a.Inspection ScopeThe inspector observed a non-exempt radioactive material shipment (PM-07-057) inpreparation. The inspector reviewed associated transportation documents, reviewed
The inspector selected and reviewed the records associated with six non-exceptedshipments of radioactive material made since the previous inspection in this area (Shipment Nos. PM-07-057, PW-07-010, PW-06-030, PW-07-007, PW-07-001, PW-07-003). The shipments were selected based on waste classification and waste-stream characteristics. The following aspects of the radioactive waste, radioactive material packaging, and radioactive material shipping activities were reviewed:*Implementation of applicable shipping requirements including completion of waste manifests;*Implementation of the specifications in applicable Certificates of Compliance, asappropriate, for the approved shipping casks including limits on package contents;*Classification and characterization of waste relative to 10 CFR 61.55 and 61.56, asappropriate;*Implementation of up-to-date NRC and Department of Transportation (DOT)shipping requirements;*Implementation of 10 CFR 20, Appendix G;
radiological surveys to support transportation, reviewed license requirements, and
discussed preparation with cognizant Exelon personnel. The inspector also reviewed
personnel training relative to
: [[NRC]] [[Bulletin 79-19 and 49]]
CFR 172, Subpart H. The
inspector reviewed and discussed technical training presented to workers. The inspector
verified that a training program was provided to personnel responsible for the conduct of
radioactive waste processing and radioactive waste shipping activities. b.FindingsNo findings of significance were identified. .5Shipment Records and Documentation   a.Inspection ScopeThe inspector selected and reviewed the records associated with six non-exceptedshipments of radioactive material made since the previous inspection in this area
(Shipment Nos.
: [[PM]] [[-07-057,]]
: [[PW]] [[-07-010,]]
: [[PW]] [[-06-030,]]
PW-07-007, PW-07-001,
PW-07-003). The shipments were selected based on waste classification and
waste-stream characteristics. The following aspects of the radioactive waste, radioactive
material packaging, and radioactive material shipping activities were reviewed:*Implementation of applicable shipping requirements including completion of waste manifests;*Implementation of the specifications in applicable Certificates of Compliance, asappropriate, for the approved shipping casks including limits on package contents;*Classification and characterization of waste relative to
: [[10 CFR]] [[61.55 and 61.56, asappropriate;*Implementation of up-to-date]]
NRC and Department of Transportation (DOT)shipping requirements;*Implementation of 10 CFR 20, Appendix G;
*Implementation of specific radioactive material shipping requirements;
*Implementation of specific radioactive material shipping requirements;
*Packaging of shipments;
*Packaging of shipments;
Line 487: Line 265:
*Evaluation of package against package performance standards, as appropriate;
*Evaluation of package against package performance standards, as appropriate;
*Conformance with procedures for cask loading, closure and use requirementsincluding consistency with cask vendor approved procedures; and*Use of latest revision documents.
*Conformance with procedures for cask loading, closure and use requirementsincluding consistency with cask vendor approved procedures; and*Use of latest revision documents.
13EnclosureThe review was against criteria contained in
 
: [[10 CFR]] [[20; 10]]
13EnclosureThe review was against criteria contained in 10 CFR 20; 10 CFR 61; 10 CFR 71;applicable DOT requirements, as contained in 49 CFR 170-189 for the above areas; station procedures; applicable disposal facility licenses; and applicable Certificates ofCompliance or vendor procedures for various shipping casks.The inspector also selectively reviewed the 2006 Annual Radioactive Effluent ReleaseReport, relative to types and quantities of radioactive waste shipped offsite and relative to changes to the PCP.
: [[CFR]] [[61;]]
 
: [[10 CFR]] [[71;applicable]]
====b. Findings====
DOT requirements, as contained in 49 CFR 170-189 for the above areas;
No findings of significance were identified..6 Audits and Assessments of Radioactive Waste Handling
station procedures; applicable disposal facility licenses; and applicable Certificates ofCompliance or vendor procedures for various shipping casks.The inspector also selectively reviewed the 2006 Annual Radioactive Effluent ReleaseReport, relative to types and quantities of radioactive waste shipped offsite and relative to
 
changes to the
====a. Inspection Scope====
: [[PCP.]] [[b.FindingsNo findings of significance were identified..6 Audits and Assessments of Radioactive Waste Handling a.Inspection ScopeThe inspector reviewed audits and assessments of the radioactive waste handling,processing, storage, and shipping programs, including the]]
The inspector reviewed audits and assessments of the radioactive waste handling,processing, storage, and shipping programs, including the PCP. The inspector also reviewed selected corrective action documents written since the previous inspection. The following documents were reviewed:*Chemistry, Radwaste, and Process Control Audit, (NOSA-PEA-06-04 (IR 476157),May 3, 2006; *Self-Assessment, ASSA-565928 A05, May 14, 2007; and  
PCP. The inspector also
*Issue Reports (IRs) 632879, 626897, 626873, 618653, 612012, 605803,592478486694, 240959, 642483, 642097, 642491, 632526, 486694. The review was against criteria contained in 10 CFR 20 Appendix G, 10 CFR 71.101, andapplicable station audit and surveillance procedures.
reviewed selected corrective action documents written since the previous inspection. The
 
following documents were reviewed:*Chemistry, Radwaste, and Process Control Audit, (NOSA-PEA-06-04 (IR 476157),May 3, 2006; *Self-Assessment,
====b. Findings====
: [[AS]] [[]]
No findings of significance were identified.4.OTHER ACTIVITIESCornerstones:  Barrier Integrity & Emergency Preparedness 4OA1Performance Indicator (PI) Verification (71151 - 7 Samples)
SA-565928 A05, May 14, 2007; and  
 
*Issue Reports (IRs) 632879, 626897, 626873, 618653, 612012, 605803,592478486694, 240959, 642483, 642097, 642491, 632526, 486694. The review was against criteria contained in
===.1 Barrier Integrity PIs ( 71151 - 4 Samples)===
: [[10 CFR]] [[20 Appendix G, 10]]
 
: [[CFR]] [[71.101, andapplicable station audit and surveillance procedures. b.FindingsNo findings of significance were identified.4.OTHER]]
====a. Inspection Scope====
: [[ACTIVI]] [[]]
The inspectors reviewed a sample of PBAPS's submittals for the four Barrier Integrity PIslisted below to verify the accuracy of the data reported. The PI definitions and the guidance contained in Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment Indicator Guideline," Revision 4, and Exelon procedure LS-AA-2001, "Collecting and 14EnclosureReporting of NRC Performance Indicator Data," were used to verify that the reportingrequirements were met. The inspectors reviewed raw PI data collected since January 2006 to December 2006 and compared graphical representations from the most recent PI report to the raw data to verify the data was included in the report. The PIs reviewed were:*Unit 2 and Unit 3 RCS Specific Activity; and*Unit 2 and Unit 3 RCS Leakage.
: [[TIESC]] [[ornerstones:  Barrier Integrity & Emergency Preparedness]]
 
: [[4OA]] [[1Performance Indicator (]]
====b. Findings====
PI) Verification (71151 - 7 Samples)  
No findings of significance were identified..2Emergency Preparedness (EP) PIs (71151 - 3 Samples)
.1Barrier Integrity
 
: [[PI]] [[s ( 71151 - 4 Samples) a.Inspection ScopeThe inspectors reviewed a sample of]]
====a. Inspection Scope====
: [[PBAPS]] [['s submittals for the four Barrier Integrity]]
The inspectors reviewed data for the following EP PIs:
: [[PI]] [[slisted below to verify the accuracy of the data reported. The]]
PI definitions and the
guidance contained in Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment
Indicator Guideline," Revision 4, and Exelon procedure
: [[LS]] [[-]]
AA-2001, "Collecting and
14EnclosureReporting of
: [[NRC]] [[Performance Indicator Data," were used to verify that the reportingrequirements were met. The inspectors reviewed raw]]
PI data collected since
January 2006 to December 2006 and compared graphical representations from the most
recent
: [[PI]] [[report to the raw data to verify the data was included in the report. The]]
PIs
reviewed were:*Unit 2 and Unit
: [[3 RCS]] [[Specific Activity; and*Unit 2 and Unit 3]]
: [[RCS]] [[Leakage. b.FindingsNo findings of significance were identified..2Emergency Preparedness (EP)]]
: [[PI]] [[s (71151 - 3 Samples) a.Inspection ScopeThe inspectors reviewed data for the following]]
EP PIs:
*Drill and Exercise Performance (DEP);*ERO Drill Participation; and
*Drill and Exercise Performance (DEP);*ERO Drill Participation; and
*ANS Reliability. The inspectors reviewed supporting documentation from drills and tests from April 2006through March 2007, to verify the accuracy of the reported data. The review of these PIs
*ANS Reliability. The inspectors reviewed supporting documentation from drills and tests from April 2006through March 2007, to verify the accuracy of the reported data. The review of these PIs was conducted in accordance with NRC IP 71151. The acceptance criteria used for the review were 10 CFR 50.9 and NEI 99-02, Revision 4, "Regulatory Assessment Performance Indicator Guidelines."
was conducted in accordance with
 
: [[NRC]] [[]]
====b. Findings====
IP 71151. The acceptance criteria used for the
No findings of significance were identified.4OA2Identification and Resolution of Problems (71152 - 1 Sample)
review were
 
: [[10 CFR]] [[50.9 and]]
===.1 Routine Review of Items Entered Into the CAP===
NEI 99-02, Revision 4, "Regulatory Assessment
 
Performance Indicator Guidelines."   b.FindingsNo findings of significance were identified.4OA2Identification and Resolution of Problems (71152 - 1 Sample) .1Routine Review of Items Entered Into the
====a. Inspection Scope====
: [[CAP]] [[a.Inspection ScopeAs required by]]
As required by IP 71152, "Identification and Resolution of Problems," and in order to helpidentify repetitive equipment failures, human performance issues or program issues for follow-up, the inspectors performed routine screening of issues entered into PBAPS's CAP. This review was accomplished by selectively reviewing copies of IRs and accessing PBAPS's computerized database.
IP 71152, "Identification and Resolution of Problems," and in order to helpidentify repetitive equipment failures, human performance issues or program issues for
 
follow-up, the inspectors performed routine screening of issues entered into
====b. Findings====
: [[PBA]] [[]]
No findings of significance were identified.
: [[PS]] [['s]]
 
: [[CAP.]] [[This review was accomplished by selectively reviewing copies of]]
15Enclosure.2Review of Operator Work-Arounds (OWAs) (71152 - 1 Work-Around Sample)
: [[IR]] [[s and accessing]]
 
: [[PBA]] [[]]
====a. Inspection Scope====
PS's computerized database. b.FindingsNo findings of significance were identified.
As required by IP 71152, "Identification and Resolution of Problems," the inspectorsconducted a review of the OWA program to verify that PBAPS was identifying OWAs problems at an appropriate threshold, have entered them in the CAP, and proposed or implemented appropriate corrective actions. The inspectors reviewed the list of OWAs and operator challenges (OCs) identified and managed in accordance with Exelon procedure, OP-AA-102-103, "Operator Work-Around Program."  Specifically, the review was conducted to determine if any OWAs for mitigating systems affected the mitigating system's safety functions or affected the operator's ability to implement abnormal and emergency operating procedures. The inspectors reviewed the following open OWAs being tracked by PBAPS:*Unit 3 Steam Jet-Air Ejector (SJAE) Suction Valves Fail to Open When Placing theSJAE In-Service (Action Request (AR) A1536806).The inspectors also reviewed the lists of open OCs (deficiencies that are obstacles tonormal plant operations), periodically walked down the panels in the main control room, and reviewed control room deficiencies to identify and be cognizant of:
15Enclosure.2Review of Operator Work-Arounds (OWAs) (71152 - 1 Work-Around Sample) a.Inspection ScopeAs required by
: (1) OWAs that have not been evaluated by PBAPS, and
: [[IP]] [[71152, "Identification and Resolution of Problems," the inspectorsconducted a review of the]]
: (2) OWAs that increase the potential for personnel error, including OWAs that: *Require operations contrary to past training or require more detailed knowledge ofthe system than routinely provided; *Require a change from longstanding operational practices;
: [[OWA]] [[program to verify that]]
: [[PBAPS]] [[was identifying]]
OWAs
problems at an appropriate threshold, have entered them in the CAP, and proposed or
implemented appropriate corrective actions. The inspectors reviewed the list of OWAs
and operator challenges (OCs) identified and managed in accordance with Exelon
procedure,
: [[OP]] [[-]]
AA-102-103, "Operator Work-Around Program."  Specifically, the review
was conducted to determine if any OWAs for mitigating systems affected the mitigating
system's safety functions or affected the operator's ability to implement abnormal and
emergency operating procedures. The inspectors reviewed the following open OWAs
being tracked by
: [[PBAPS]] [[:*Unit 3 Steam Jet-Air Ejector (]]
SJAE) Suction Valves Fail to Open When Placing theSJAE In-Service (Action Request (AR) A1536806).The inspectors also reviewed the lists of open OCs (deficiencies that are obstacles tonormal plant operations), periodically walked down the panels in the main control room,
and reviewed control room deficiencies to identify and be cognizant of: (1) OWAs that
have not been evaluated by
: [[PBAPS]] [[, and (2)]]
OWAs that increase the potential for
personnel error, including OWAs that: *Require operations contrary to past training or require more detailed knowledge ofthe system than routinely provided; *Require a change from longstanding operational practices;
*Require operation of a system or component in a manner dissimilar from similarsystems or components;*Create the potential for the compensatory action to be performed on equipment orunder conditions for which it is not appropriate;*Impair access to required indications, increase dependence on oralcommunications, or require actions under adverse environmental conditions; and*Require the use of equipment and interfaces that had not been designed withconsideration of the task being performed.
*Require operation of a system or component in a manner dissimilar from similarsystems or components;*Create the potential for the compensatory action to be performed on equipment orunder conditions for which it is not appropriate;*Impair access to required indications, increase dependence on oralcommunications, or require actions under adverse environmental conditions; and*Require the use of equipment and interfaces that had not been designed withconsideration of the task being performed.
b.FindingsNo findings of significance were identified..3Semi-Annual Review to Identify Trends (71152 - 1 Semi-annual Trend Sample)  .aInspection ScopeAs required by
 
: [[IP]] [[71152, Identification and Resolution of Problems, the inspectorsreviewed a list of approximately 5,000]]
====b. Findings====
: [[IR]] [[s that Exelon initiated at]]
No findings of significance were identified..3Semi-Annual Review to Identify Trends (71152 - 1 Semi-annual Trend Sample)  .aInspection ScopeAs required by IP 71152, Identification and Resolution of Problems, the inspectorsreviewed a list of approximately 5,000 IRs that Exelon initiated at PBAPS from December 1, 2006 through June 1, 2007, to perform the semi-annual PI&R trend review.
: [[PBA]] [[]]
 
PS from December
Approximately, 30 IRs were reviewed in detail to verify that the issues were adequately identified, appropriately evaluated and corrected. The inspectors review was focused on 16Enclosurehuman performance issues. The review also included issues documented within PBAPS'sStation Trend Review for the fourth quarter of 2006 and the first quarter of 2007.
1, 2006 through June 1, 2007, to perform the semi-annual PI&R trend review.
 
Approximately, 30 IRs were reviewed in detail to verify that the issues were adequately
b.Assessments and ObservationsAlthough no findings of significance were identified, the inspectors observed that the plantis being challenged by human performance deficiencies. Specifically, procedure adherence was the aspect of human performance that was most frequently challenged.
identified, appropriately evaluated and corrected. The inspectors review was focused on
 
16Enclosurehuman performance issues. The review also included issues documented within
Examples are documented in IRs 568038, 577381, 581258, 604364, 596616, 626534 and 633532. Procedure quality was another aspect of human performance that was challenged. Examples are documented in IRs 635028, 633532, and 600686. However, the inspectors did not identify any new trends that were not previously identified by PBAPS under their quarterly Station Trend Review reports. The inspectors noted that the Station Trend Review report had identified procedure adherence issues as an emerging trend. The inspectors also noted that improving human performance was identified as one of five Station Focus areas for 2007.4OA3Event Followup (71153 - 5 Samples)
: [[PBA]] [[]]
 
PS'sStation Trend Review for the fourth quarter of 2006 and the first quarter of 2007. b.Assessments and ObservationsAlthough no findings of significance were identified, the inspectors observed that the plantis being challenged by human performance deficiencies. Specifically, procedure
===.1 (Closed) Unresolved Item (URI) 05000277/2007002-04, Incorrect Size Breaker Resultedin a Fire in the '4T4' 480 Volt Load Center===
adherence was the aspect of human performance that was most frequently challenged.
 
Examples are documented in IRs 568038, 577381, 581258, 604364, 596616, 626534 and
====a. Inspection Scope====
633532. Procedure quality was another aspect of human performance that was
URI 05000277/2007002-04 was opened in NRC Inspection Report 050000277;05000278/2007002. PBAPS had preliminarily determined that the fire resulted from an apparent mismatch between the ratings of one breaker and its cubicle in the '4T4' 480 volt load center. PBAPS's report also documented that operators responded to the equipment losses caused by the fire by initiating a transient of controlled reactor power reductions to stabilize the plant at approximately 50 percent of rated power. The URI was opened pending the NRC staffs' characterization of this issue following review of PBAPS's causal evaluation and corrective actions. PBAPS's root cause report (RCR) and the associated IR 596616 for this event were reviewed to assess the identified issues. The characterization of this issue as a finding and its risk significance are discussed below.
challenged. Examples are documented in IRs 635028, 633532, and 600686. However,
 
the inspectors did not identify any new trends that were not previously identified by
This URI is closed.
: [[PBA]] [[]]
 
PS under their quarterly Station Trend Review reports. The inspectors noted that the
====b. Findings====
Station Trend Review report had identified procedure adherence issues as an emerging
 
trend. The inspectors also noted that improving human performance was identified as
=====Introduction.=====
one of five Station Focus areas for 2007.4OA3Event Followup (71153 - 5 Samples) .1(Closed) Unresolved Item (URI) 05000277/2007002-04, Incorrect Size Breaker Resultedin a Fire in the '4T4' 480 Volt Load Center a.Inspection ScopeURI 05000277/2007002-04 was opened in
A Green self-revealing finding was identified for inadequate implementationof WO instructions to verify the correct breaker frame size during the overhaul of a compatible spare breaker for installation into the '4T4' 480 volt load center. This condition resulted in a poor electrical connection between the primary disconnect fingers and the switchgear bus stabs for one breaker in the '4T4' load center that ultimately resulted in a fire that led to a plant transient and declaration of an Unusual Event (UE).Description. On February 27, 2007, operators reduced Unit 3 reactor power from 100percent to 50 percent RTP in response to the effects of a fire in the '4T4' 480 volt load center. PBAPS's RCR stated that the fire was caused by an electrical fault in one breaker cubicle that occurred due to a poor electrical connection between the breaker primary 17Enclosuredisconnect fingers and the switchgear bus stabs. This poor electrical connection resultedfrom a configuration error that placed the wrong frame size breaker into the cubicle in the
: [[NRC]] [[Inspection Report 050000277;05000278/2007002.]]
'4T4' 480 volt load center creating a high resistance, high temperature connection.
PBAPS had preliminarily determined that the fire resulted from an
 
apparent mismatch between the ratings of one breaker and its cubicle in the '4T4' 480 volt
The RCR identified that a root cause for the configuration error was that standards,policies, and administrative controls (SPAC) were not used. Specifically, SPAC were notused, in that, the maintenance technicians did not strictly adhere to WO instructions to specifically verify the frame size during the overhaul of a spare breaker that was intended to be placed into the breaker cubicle. The inspectors determined that this issue was a performance deficiency becausemaintenance technicians did not follow WO instructions to verify the correct breaker frame size during the overhaul of a spare breaker.  
load center.
 
: [[PBA]] [[]]
=====Analysis.=====
PS's report also documented that operators responded to the equipment
This finding is greater than minor because it affected the human performanceattribute of the Initiating Event Cornerstone, in that, the incorrect frame size breaker was installed in cubicle for which it was not sized. This mismatch caused an electrical fault that led to a fire and a transient that upset plant stability.
losses caused by the fire by initiating a transient of controlled reactor power reductions to
 
stabilize the plant at approximately 50 percent of rated power. The URI was opened
The inspectors evaluated the finding in accordance with IMC 0609, Appendix A, "SDP ofReactor Inspection Findings for At-Power Situations."  The SDP Phase 1 screeningidentified that the finding was of very low safety significance (Green) because it did not increase both the likelihood of a reactor scram and that mitigation equipment or functions would not be available. The inspectors determined that this finding had a cross-cutting aspect in the area ofhuman performance (work practices component) because maintenance technicians did not follow  WO instructions to specifically verify the frame size of a breaker during its overhaul (IMC 0305 aspect H.4(b)).
pending the
 
: [[NRC]] [[staffs' characterization of this issue following review of]]
=====Enforcement.=====
PBAPS's causal
The inspectors determined that the finding did not represent a violation ofregulatory requirements because it involved the '4T4' 480 volt load center, a non-safety related electrical bus. This finding will be tracked as FIN 05000278/2007003-01, Inadequate Implementation of Work Order Instructions Caused the Installation of an Incorrect Size Breaker and Resulted in a Fire in the '4T4' 480 Volt Load Center.2(Closed) URI 05000277/2007002-05, Missed Procedure Step Resulted in UnplannedOverloading of the E-3 EDGURI 05000277/2007002-05 was opened in NRC Inspection Report 050000277;05000278/2007002, pending the NRC staffs' characterization of this issue following a review of PBAPS's root cause analyses, corrective actions taken or planned, approved procedures, and other documents. The characterization of this issue as a finding and its risk significance are discussed below. This URI is closed.
evaluation and corrective actions.
 
: [[PBAPS]] [['s root cause report (]]
====b. Findings====
RCR) and the associated
 
IR 596616 for this event were reviewed to assess the identified issues. The
=====Introduction.=====
characterization of this issue as a finding and its risk significance are discussed below.
A self-revealing (Green) NCV of Technical Specification (TS) 5.4.1, wasidentified when operators inadequately implemented a surveillance test by missing a 18Enclosureprocedure step. The missed step placed the E-3 EDG in the isochronous mode ofoperation while it was synchronized to off-site power and resulted in an unexpected over-loading of the E-3 EDG.  
This
 
: [[URI]] [[is closed. b.FindingsIntroduction. A Green self-revealing finding was identified for inadequate implementationof]]
=====Description.=====
WO instructions to verify the correct breaker frame size during the overhaul of a
During the conduct of a E-3 EDG ST on March 15, 2007, a licensed operatormissed the performance of a required step in a supporting system operating (SO)procedure. The omission of the procedure step placed the E-3 EDG in the isochronous mode while synchronized with off-site power through a 4 kilovolt (kV) vital bus. This condition resulted in unexpectedly loading the E-3 EDG beyond its 30-minute load rating.
compatible spare breaker for installation into the '4T4' 480 volt load center. This condition
 
resulted in a poor electrical connection between the primary disconnect fingers and the
The ST-O-052-123-2, "E3 Diesel Generator RHR Pump Reject Test," and the supporting SO 52.A.1.B, "Diesel Generator Operations," directed the synchronization of the E-3 EDG, in the droop mode, to a selected 4 kV bus to pick up the bus loads. The SO 52.A.1.B procedure subsequently directed opening the off-site power feeder breaker to the 4 kV vital bus (the missed step) before placing the EDG in the isochronous mode in accordance with ST-O-052-123-2. The inspectors reviewed PBAPS's root cause investigation report (IR 604364) tounderstand the underlying causes for this event. The inspectors noted that PBAPS identified two root causes for this self-revealing event. First, the plant reactor operator (PRO) did not adhere to the requirements of HU-AA-104-101, "Procedure Use and Adherence" for "Level 1 - Continuous Use," procedures which requires that each procedure step be read prior to being performed, performing each step in the sequence specified, and signing off each step as complete prior to proceeding to the next step.
switchgear bus stabs for one breaker in the '4T4' load center that ultimately resulted in a
 
fire that led to a plant transient and declaration of an Unusual Event (UE).Description. On February 27, 2007, operators reduced Unit 3 reactor power from 100percent to 50 percent RTP in response to the effects of a fire in the '4T4' 480 volt load
Specifically, procedure adherence broke down because the PRO allowed himself to be distracted and lost his place in SO 52.A.1.B. Therefore, the off-site feeder breaker to the E-33 bus was not opened in accordance with the SO prior to transferring the E-3 EDG to the isochronous load control mode per the ST.The second root cause for this event was inadequate supervisory oversight during acritical transition between the ST and SO procedures. Specifically, the peer checker and the control room supervisor were not directly observing the operation of the E-3 EDG at the main control room panel during the critical transition between procedures. The transition between procedures should have been identified as a critical step in the testing evolution. This breakdown in crew teamwork resulted in the PRO performing a critical step, without direct oversight, during an infrequently performed test of safety-related equipment. As a result, no one challenged the PRO's decision to transfer the E-3 EDG to the isochronous load control mode when system conditions did not support it.Based on the above, the inspectors determined that inadequately implementing asurveillance test by missing a procedure step was a performance deficiency.  
center.
 
: [[PBAPS]] [['s]]
=====Analysis.=====
RCR stated that the fire was caused by an electrical fault in one breaker
The inspectors concluded the finding was more than minor because it wasassociated with the human performance attribute of the Mitigating Systems Cornerstone, and impacted the cornerstone objective of ensuring the availability of E-3 EDG to respond to initiating events, in that, after the EDG was overloaded, additional unavailability was incurred to inspect the EDG for damage before it was returned to service. The E-3 EDG was inoperable for an additional 46 hours and was unavailable for an additional 12.5hours. Traditional enforcement does not apply since there were no actual safety 19Enclosureconsequences or potential for impacting the NRC's regulatory function, and the findingwas not the result of any willful violation of NRC requirements.
cubicle that occurred due to a poor electrical connection between the breaker primary
 
17Enclosuredisconnect fingers and the switchgear bus stabs. This poor electrical connection resultedfrom a configuration error that placed the wrong frame size breaker into the cubicle in the
The inspectors completed a significance determination of this issue using IMC 0609,"SDP," Appendix A, "Determining the Significance of Reactor Inspection Findings for At-Power Situations."  The inspectors concluded that this finding affected the Mitigating Systems Cornerstone and answered "No" to all relevant questions. Specifically, all other EDGs remained operable and the actual loss of safety function for E-3 EDG was shorter than its TS allowed outage time of seven days. Therefore, this finding was considered to be of very low safety significance (Green).The inspectors determined that this finding had a cross-cutting aspect in the area ofhuman performance (work practices component) because PBAPS personnel did not follow procedures when the E-3 EDG was placed in the isochronous load control mode with the E-3 EDG in parallel with the off-site power source.  (IMC 0305 aspect H.4(b))Enforcement. TS 5.4.1 requires that procedures be implemented covering the activities inRegulatory Guide (RG) 1.33. RG 1.33, Appendix A, Section H.2.b requires that surveillance procedures be developed for testing EDGs.
'4T4' 480 volt load center creating a high resistance, high temperature connection. The
 
: [[RCR]] [[identified that a root cause for the configuration error was that standards,policies, and administrative controls (]]
Applicable ST-O-052-123-2, Step 6.3.1, instructed the operators to synchronize and load the E-3 EDG to the 4 kV bus being tested in accordance with SO 52A.1.B. Step 4.4.16 of SO 52A.1.B directed the operators to open the off-site power source feeder breaker to the E-33 bus before placing the EDG controls in the isochronous load control mode. Contrary to the above, on March 15, 2007, operators missed SO 52A.1.B, Step 4.4.16,and did not open the applicable off-site power breaker before returning to ST-O-052-123-2, Step 6.3.2. Therefore, when the PRO placed the E-3 EDG in the isochronous load control mode in Step 6.3.2, there was an unexpected increase in E-3 EDG load and a trip of the E-3 EDG output breaker.PBAPS placed this issue in the CAP by initiating IR 604364. The corrective actions forthis event included:  1) the selective implementation of additional peer checking of procedure performance place-keeping; and, 2) the E-3 EDG was inspected for potential damage and tested before being returned to an operable status on March 17, 2007.
: [[SPAC]] [[) were not used. Specifically,]]
 
: [[SPAC]] [[were notused, in that, the maintenance technicians did not strictly adhere to]]
Because this violation was of very low safety significance (Green) and documented in PBAPS's CAP as IR 604364, this finding is being treated as an NCV, consistent withSection VI.A of the NRC Enforcement Policy:  NCV 05000277/2007003-02;05000278/2007003-02, Missed Procedure Step Resulted in Unplanned Overloading of the E-3 EDG
WO instructions to
..3Personnel Performance - Failure of DDFP
specifically verify the frame size during the overhaul of a spare breaker that was intended
 
to be placed into the breaker cubicle. The inspectors determined that this issue was a performance deficiency becausemaintenance technicians did not follow WO instructions to verify the correct breaker frame
====a. Inspection Scope====
size during the overhaul of a spare breaker. Analysis. This finding is greater than minor because it affected the human performanceattribute of the Initiating Event Cornerstone, in that, the incorrect frame size breaker was
The inspectors reviewed corrective action documents listed in the Attachment to thisreport, and discussed the events surrounding the failure of the DDFP with the site fire protection engineer. The inspectors reviewed Revisions 10 and 12 of ST-O-37D-340-2, "DDFP Flow Rate Test," and Revision 2 of NOM-C-7.1, "Procedure Use."
installed in cubicle for which it was not sized. This mismatch caused an electrical fault
 
that led to a fire and a transient that upset plant stability. The inspectors evaluated the finding in accordance with
====b. Findings====
: [[IMC]] [[0609, Appendix A, "]]
 
SDP ofReactor Inspection Findings for At-Power Situations."  The SDP Phase 1 screeningidentified that the finding was of very low safety significance (Green) because it did not
=====Introduction.=====
increase both the likelihood of a reactor scram and that mitigation equipment or functions
A self-revealing Green NCV was identified for failure to comply with TS5.4.1, "Procedures," which required that procedures be established, implemented, and maintained for the Fire Protection Program.
would not be available. The inspectors determined that this finding had a cross-cutting aspect in the area ofhuman performance (work practices component) because maintenance technicians did
 
not follow  WO instructions to specifically verify the frame size of a breaker during its
=====Description.=====
overhaul (IMC 0305 aspect H.4(b)). Enforcement. The inspectors determined that the finding did not represent a violation ofregulatory requirements because it involved the '4T4' 480 volt load center, a non-safety
PBAPS TS 5.4.1.a, requires that procedures be established, implementedand maintained  as recommended in Appendix A to RG 1.33, dated November 1972.
related electrical bus. This finding will be tracked as FIN 05000278/2007003-01,
 
Inadequate Implementation of Work Order Instructions Caused the Installation of an
RG 1.33, Appendix A, Section 1, "Administrative Procedures," includes the fire protection program. The Nuclear Operations Manual (NOM)-C-7.1, "Procedure Use," requires that procedures be used for any task which has the potential to cause a system or component to become inoperable.On May 23, 2007, during performance of ST-O-37D-340-2, the DDFP was declaredinoperable due to low discharge pressure. After running the DDFP, the procedure directed cleaning of the cooling water strainer, but did not provide specific instructions on how to perform this task. Without procedure guidance or instructions, operations personnel performing the DDFP test closed an upstream hand valve to isolate the strainer for cleaning. After reassembling the strainer, the operations personnel did not re-open the hand valve. The cooling water was not properly realigned for service because equipment manipulations were performed outside of procedure guidance. On May 24, 2007, ST-O-37D-340-2 was re-performed with the cooling water supply isolated. The engine was damaged during operation without cooling water as a result of the valve mis-alignment. The DDFP was subsequently returned to service on May 30, 2007, following repairs. Additionally, the DDFP flow rate test procedure was revised to include specific instructions for cleaning the cooling water strainer. The procedure was also revised to include instructions for monitoring the engine cooling water and lubricating oil parameters during engine operation. Based on the above, the inspectors determined that manipulating the DDFP cooling watervalve without procedure guidance was a performance deficiency.  
Incorrect Size Breaker and Resulted in a Fire in the '4T4' 480 Volt Load Center.2(Closed)
 
: [[URI]] [[05000277/2007002-05, Missed Procedure Step Resulted in UnplannedOverloading of the E-3]]
=====Analysis.=====
: [[EDGURI]] [[05000277/2007002-05 was opened in]]
The inspectors concluded that the failure to use a procedure for cleaning andrestoring the DDFP cooling water strainer was a more than minor finding because it was associated with the degradation of a fire protection feature, in that, the DDFP was rendered inoperable by damage to the engine. Traditional enforcement does not apply since there were no actual safety consequences or potential for impacting the NRC's regulatory function, and the finding was not the result of any willful violation of NRC requirements.
: [[NRC]] [[Inspection Report 050000277;05000278/2007002, pending the]]
 
NRC staffs' characterization of this issue following a
The inspectors assessed the finding using the Fire Protection SDP (Appendix F to IMC 0609) and determined the finding to be of very low safety significance (Green). The finding was of low significance due to the motor-driven fire pump remaining operable during the five days the DDFP was inoperable, and the small number of fire scenarios which would impact the power supply to the motor-driven fire pump.
review of
 
: [[PBA]] [[]]
21EnclosureThe inspectors determined that this finding had a cross-cutting aspect in the area ofhuman performance (resources component) because procedure ST-O-37D-340-2 did not provide complete and accurate instructions for cleaning the DDFP cooling water strainer.
PS's root cause analyses, corrective actions taken or planned, approved
 
procedures, and other documents. The characterization of this issue as a finding and its
(IMC 0305 aspect H.2©)Enforcement. TS 5.4.1.a and NOM-C-7.1 require that procedures be used for equipmentmanipulations which could cause fire protection components to become inoperable.
risk significance are discussed below. This
 
: [[URI]] [[is closed. b.FindingsIntroduction. A self-revealing (Green)]]
Contrary to the above, procedures were not used when manipulating the DDFP cooling water isolation valves on May 23, 2007, resulting in the DDFP being run on May 24, 2007, without cooling water and sustaining engine damage. Because this failure to comply with TS 5.4.1.a is of very low safety significance (Green) and has been entered into PBAPS's CAP as IR 633532, this violation is being treated as an NCV, consistent with Section VI.Aof the NRC Enforcement Policy: NCV 05000277, 278/2007003-03, InadequateProcedure Adherence Results in Damage to the DDFP
NCV of Technical Specification (TS) 5.4.1, wasidentified when operators inadequately implemented a surveillance test by missing a
..4(Closed) Licensee Event Report (LER) 05000277/2006002-00, AutomaticDepressurization System (ADS) SRV DeficienciesOn September 28, 2006, engineering personnel determined that the 71B and 71G SRVsdid not meet their allowable leak rate for the pneumatic actuation controls for the ADS feature of the SRVs. Additionally, the 71C SRV, Serial Number 9S/N 83, did not properly re-close on the fourth actuation during laboratory testing. The cause of the 71B and 71G ADS SRV pneumatic leakage is attributed to leakage from each of the SRV's actuator diaphragm and solenoid valve. These leaks only occurred when the SRV solenoid valveswere energized. The diaphragms and solenoid valves associated with the 71B and 71G ADS SRVs were replaced under work orders C0219044 and C0219034. As-left leak testing was performed and the values were restored to an operable condition prior to plant startup from the P2R16 Refueling Outage. A refurbished SRV was installed in the 71C SRV location to replace the S/N 83 SRV. The corrective actions to resolve the underlying causes of this event are in the CAP (IR 539277). This licensee-identified violation was more than minor since it was associated with theEquipment Performance attribute of the Mitigating Systems Cornerstone and impacts the cornerstone objective of ensuring the reliability, availability, and capability of systems that respond to initiating events, in that, if the ADS system was called upon to actuate it's operability would not be ensured. The inspectors evaluated this finding using IMC 0609, Appendix A, "SDP of Reactor Inspector Findings for At-Power Situations," Phase 1 screening. Specifically, using the Mitigating Systems Cornerstone column, the inspectors determined that a Phase 2 evaluation was required because the finding represented a loss of system safety function. The inspectors concluded that the finding was of very low safety significance (Green) because the success criteria for depressurization, on each of the applicable worksheets, only required the use of 2 of 11 SRVs. A regional senior reactor analyst reviewed and concurred with the inspectors risk assessment. This licensee-identified finding involved a violation of TS 3.5.1, "Emergency Core Cooling Systems."  The enforcement aspects of this violation are discussed in Section
18Enclosureprocedure step. The missed step placed the E-3 EDG in the isochronous mode ofoperation while it was synchronized to off-site power and resulted in an unexpected over-
{{a|4OA7}}
loading of the E-3
==4OA7 of==
: [[EDG.]] [[Description. During the conduct of a E-3]]
 
: [[EDG]] [[]]
: [[ST]] [[on March 15, 2007, a licensed operatormissed the performance of a required step in a supporting system operating (]]
SO)
procedure. The omission of the procedure step placed the E-3 EDG in the isochronous
mode while synchronized with off-site power through a 4 kilovolt (kV) vital bus. This
condition resulted in unexpectedly loading the E-3 EDG beyond its 30-minute load rating.
The
: [[ST]] [[-O-052-123-2, "E3 Diesel Generator]]
: [[RHR]] [[Pump Reject Test," and the supporting]]
: [[SO]] [[52.A.1.B, "Diesel Generator Operations," directed the synchronization of the E-3]]
EDG,
in the droop mode, to a selected 4 kV bus to pick up the bus loads. The SO 52.A.1.B
procedure subsequently directed opening the off-site power feeder breaker to the 4 kV
vital bus (the missed step) before placing the EDG in the isochronous mode in
accordance with
: [[ST]] [[-O-052-123-2. The inspectors reviewed]]
: [[PBAPS]] [['s root cause investigation report (IR 604364) tounderstand the underlying causes for this event. The inspectors noted that]]
: [[PBA]] [[]]
PS
identified two root causes for this self-revealing event. First, the plant reactor operator
(PRO) did not adhere to the requirements of
: [[HU]] [[-]]
AA-104-101, "Procedure Use and
Adherence" for "Level 1 - Continuous Use," procedures which requires that each
procedure step be read prior to being performed, performing each step in the sequence
specified, and signing off each step as complete prior to proceeding to the next step.
Specifically, procedure adherence broke down because the PRO allowed himself to be
distracted and lost his place in SO 52.A.1.B. Therefore, the off-site feeder breaker to the
E-33 bus was not opened in accordance with the
: [[SO]] [[prior to transferring the E-3]]
EDG to
the isochronous load control mode per the
: [[ST.T]] [[he second root cause for this event was inadequate supervisory oversight during acritical transition between the]]
ST and SO procedures. Specifically, the peer checker and
the control room supervisor were not directly observing the operation of the E-3 EDG at
the main control room panel during the critical transition between procedures. The
transition between procedures should have been identified as a critical step in the testing
evolution. This breakdown in crew teamwork resulted in the PRO performing a critical
step, without direct oversight, during an infrequently performed test of safety-related
equipment. As a result, no one challenged the
: [[PRO]] [['s decision to transfer the E-3]]
EDG to
the isochronous load control mode when system conditions did not support it.Based on the above, the inspectors determined that inadequately implementing asurveillance test by missing a procedure step was a performance deficiency. Analysis. The inspectors concluded the finding was more than minor because it wasassociated with the human performance attribute of the Mitigating Systems Cornerstone,
and impacted the cornerstone objective of ensuring the availability of E-3 EDG to respond
to initiating events, in that, after the EDG was overloaded, additional unavailability was
incurred to inspect the
: [[EDG]] [[for damage before it was returned to service. The E-3]]
EDG
was inoperable for an additional 46 hours and was unavailable for an additional 12.5hours. Traditional enforcement does not apply since there were no actual safety
19Enclosureconsequences or potential for impacting the
: [[NRC]] [['s regulatory function, and the findingwas not the result of any willful violation of]]
: [[NRC]] [[requirements. The inspectors completed a significance determination of this issue using]]
: [[IMC]] [[0609,"]]
SDP," Appendix A, "Determining the Significance of Reactor Inspection Findings for
At-Power Situations."  The inspectors concluded that this finding affected the Mitigating
Systems Cornerstone and answered "No" to all relevant questions. Specifically, all other
: [[EDG]] [[s remained operable and the actual loss of safety function for E-3]]
EDG was shorter
than its TS allowed outage time of seven days. Therefore, this finding was considered to
be of very low safety significance (Green).The inspectors determined that this finding had a cross-cutting aspect in the area ofhuman performance (work practices component) because
: [[PBA]] [[]]
PS personnel did not
follow procedures when the E-3 EDG was placed in the isochronous load control mode
with the E-3
: [[EDG]] [[in parallel with the off-site power source.  (]]
: [[IMC]] [[0305 aspect]]
: [[H.]] [[4(b))Enforcement.]]
TS 5.4.1 requires that procedures be implemented covering the activities inRegulatory Guide (RG) 1.33. RG 1.33, Appendix A, Section H.2.b requires that
surveillance procedures be developed for testing
: [[EDG]] [[s. Applicable]]
ST-O-052-123-2,
Step 6.3.1, instructed the operators to synchronize and load the E-3 EDG to the 4 kV bus
being tested in accordance with
: [[SO]] [[52A.1.B. Step 4.4.16 of]]
SO 52A.1.B directed the
operators to open the off-site power source feeder breaker to the E-33 bus before placing
the
: [[EDG]] [[controls in the isochronous load control mode. Contrary to the above, on March 15, 2007, operators missed]]
: [[SO]] [[52A.1.B, Step 4.4.16,and did not open the applicable off-site power breaker before returning to]]
: [[ST]] [[-O-052-123-2, Step 6.3.2. Therefore, when the]]
PRO placed the E-3 EDG in the
isochronous load control mode in Step 6.3.2, there was an unexpected increase in E-3
: [[EDG]] [[load and a trip of the E-3]]
: [[EDG]] [[output breaker.PBAPS placed this issue in the]]
: [[CAP]] [[by initiating]]
IR 604364. The corrective actions forthis event included:  1) the selective implementation of additional peer checking of
procedure performance place-keeping; and, 2) the E-3 EDG was inspected for potential
damage and tested before being returned to an operable status on March 17, 2007.
Because this violation was of very low safety significance (Green) and documented in
: [[PBAPS]] [['s]]
: [[CAP]] [[as]]
: [[IR]] [[604364, this finding is being treated as an]]
: [[NCV]] [[, consistent withSection]]
: [[VI.A]] [[of the]]
NRC Enforcement Policy:  NCV 05000277/2007003-02;05000278/2007003-02, Missed Procedure Step Resulted in Unplanned Overloading
of the E-3
: [[EDG..]] [[3Personnel Performance - Failure of]]
: [[DDFP]] [[a.Inspection ScopeThe inspectors reviewed corrective action documents listed in the Attachment to thisreport, and discussed the events surrounding the failure of the]]
: [[DD]] [[]]
FP with the site fire
protection engineer. The inspectors reviewed Revisions 10 and 12 of ST-O-37D-340-2,
"DDFP Flow Rate Test," and Revision 2 of NOM-C-7.1, "Procedure Use."
20Enclosure    b.FindingsIntroduction. A self-revealing Green
: [[NCV]] [[was identified for failure to comply with]]
TS5.4.1, "Procedures," which required that procedures be established, implemented, and
maintained for the Fire Protection Program. Description.
: [[PBAPS]] [[]]
TS 5.4.1.a, requires that procedures be established, implementedand maintained  as recommended in Appendix A to RG 1.33, dated November 1972.
RG 1.33, Appendix A, Section 1, "Administrative Procedures," includes the fire protection
program. The Nuclear Operations Manual (NOM)-C-7.1, "Procedure Use," requires that
procedures be used for any task which has the potential to cause a system or component
to become inoperable.On May 23, 2007, during performance of
: [[ST]] [[-O-37D-340-2, the]]
: [[DDFP]] [[was declaredinoperable due to low discharge pressure. After running the]]
: [[DD]] [[]]
FP, the procedure
directed cleaning of the cooling water strainer, but did not provide specific instructions on
how to perform this task. Without procedure guidance or instructions, operations
personnel performing the
: [[DD]] [[]]
FP test closed an upstream hand valve to isolate the strainer
for cleaning. After reassembling the strainer, the operations personnel did not re-open the
hand valve. The cooling water was not properly realigned for service because equipment
manipulations were performed outside of procedure guidance. On May 24, 2007,
ST-O-37D-340-2 was re-performed with the cooling water supply isolated. The engine
was damaged during operation without cooling water as a result of the valve mis-
alignment. The
: [[DDFP]] [[was subsequently returned to service on May 30, 2007, following repairs. Additionally, the]]
DDFP flow rate test procedure was revised to include specific instructions
for cleaning the cooling water strainer. The procedure was also revised to include
instructions for monitoring the engine cooling water and lubricating oil parameters during
engine operation. Based on the above, the inspectors determined that manipulating the
: [[DDFP]] [[cooling watervalve without procedure guidance was a performance deficiency. Analysis. The inspectors concluded that the failure to use a procedure for cleaning andrestoring the]]
DDFP cooling water strainer was a more than minor finding because it was
associated with the degradation of a fire protection feature, in that, the
: [[DD]] [[]]
FP was
rendered inoperable by damage to the engine. Traditional enforcement does not apply
since there were no actual safety consequences or potential for impacting the NRC's
regulatory function, and the finding was not the result of any willful violation of
: [[NRC]] [[requirements. The inspectors assessed the finding using the Fire Protection]]
: [[SDP]] [[(Appendix F to]]
IMC 0609) and determined the finding to be of very low safety significance (Green). The
finding was of low significance due to the motor-driven fire pump remaining operable
during the five days the
: [[DD]] [[]]
FP was inoperable, and the small number of fire scenarios
which would impact the power supply to the motor-driven fire pump.
21EnclosureThe inspectors determined that this finding had a cross-cutting aspect in the area ofhuman performance (resources component) because procedure ST-O-37D-340-2 did not
provide complete and accurate instructions for cleaning the
: [[DD]] [[]]
FP cooling water strainer.  
(IMC 0305 aspect
: [[H.]] [[2©)Enforcement.]]
TS 5.4.1.a and NOM-C-7.1 require that procedures be used for equipmentmanipulations which could cause fire protection components to become inoperable.
Contrary to the above, procedures were not used when manipulating the
: [[DD]] [[]]
FP cooling
water isolation valves on May 23, 2007, resulting in the
: [[DD]] [[]]
FP being run on May 24, 2007,
without cooling water and sustaining engine damage. Because this failure to comply with
: [[TS]] [[5.4.1.a is of very low safety significance (Green) and has been entered into]]
: [[PBAPS]] [['s]]
: [[CAP]] [[as]]
: [[IR]] [[633532, this violation is being treated as an]]
: [[NCV]] [[, consistent with Section]]
: [[VI.A]] [[of the]]
: [[NRC]] [[Enforcement Policy:]]
: [[NCV]] [[05000277, 278/2007003-03, InadequateProcedure Adherence Results in Damage to the]]
: [[DDFP..]] [[4(Closed) Licensee Event Report (]]
: [[LER]] [[) 05000277/2006002-00, AutomaticDepressurization System (ADS)]]
: [[SRV]] [[DeficienciesOn September 28, 2006, engineering personnel determined that the 71B and 71G]]
SRVsdid not meet their allowable leak rate for the pneumatic actuation controls for the
: [[ADS]] [[feature of the]]
: [[SRV]] [[s. Additionally, the 71C]]
SRV, Serial Number 9S/N 83, did not properly
re-close on the fourth actuation during laboratory testing. The cause of the 71B and 71G
: [[ADS]] [[]]
SRV pneumatic leakage is attributed to leakage from each of the SRV's actuator
diaphragm and solenoid valve. These leaks only occurred when the
: [[SRV]] [[solenoid valveswere energized. The diaphragms and solenoid valves associated with the 71B and 71G]]
: [[ADS]] [[]]
SRVs were replaced under work orders C0219044 and C0219034. As-left leak
testing was performed and the values were restored to an operable condition prior to plant
startup from the P2R16 Refueling Outage. A refurbished
: [[SRV]] [[was installed in the 71C]]
: [[SRV]] [[location to replace the S/N 83]]
SRV. The corrective actions to resolve the underlying
causes of this event are in the
: [[CAP]] [[(]]
IR 539277). This licensee-identified violation was more than minor since it was associated with theEquipment Performance attribute of the Mitigating Systems Cornerstone and impacts the
cornerstone objective of ensuring the reliability, availability, and capability of systems that
respond to initiating events, in that, if the ADS system was called upon to actuate it's
operability would not be ensured. The inspectors evaluated this finding using IMC 0609,
Appendix A, "SDP of Reactor Inspector Findings for At-Power Situations," Phase 1
screening. Specifically, using the Mitigating Systems Cornerstone column, the inspectors
determined that a Phase 2 evaluation was required because the finding represented a
loss of system safety function. The inspectors concluded that the finding was of very low
safety significance (Green) because the success criteria for depressurization, on each of
the applicable worksheets, only required the use of 2 of 11 SRVs. A regional senior
reactor analyst reviewed and concurred with the inspectors risk assessment. This
licensee-identified finding involved a violation of TS 3.5.1, "Emergency Core Cooling
Systems."  The enforcement aspects of this violation are discussed in Section 4OA7 of
this report. This LER is closed.
this report. This LER is closed.
2Enclosure.5(Closed)
 
: [[LER]] [[05000277/2006004-00, Plant Modification Created Diesel GeneratorBuilding Carbon Dioxide Suppression Room Flooding VulnerabilityOn November 17, 2006, engineering personnel determined that a potential floodvulnerability had existed in the]]
22Enclosure.5(Closed) LER 05000277/2006004-00, Plant Modification Created Diesel GeneratorBuilding Carbon Dioxide Suppression Room Flooding VulnerabilityOn November 17, 2006, engineering personnel determined that a potential floodvulnerability had existed in the EDG building carbon dioxide suppression room. A plant modification performed in 1985 had installed a catch basin at the EDG building fuel oil filling station, which is located outside the EDG building. The catch basin discharge was tied into the EDG building's oily waste separator tank, upstream of the flood protection isolation valve. This constituted an unanalyzed condition that degraded plant safety. In the event of a design basis flood, a potential pathway existed for flood water to enter the building through the floor drains. It was determined that the maximum credible flow rate would have exceeded the capability of the floor drain sump and sump pumps. Under design basis flood conditions, the ESW system booster pumps and return valves, and the HPSW system return valves would be challenged to perform their safety function.
EDG building carbon dioxide suppression room. A plant
 
modification performed in 1985 had installed a catch basin at the EDG building fuel oil
Corrective actions recommended for this issue were documented in IR 554800 and included revision of the applicable special event procedure for floods to mitigate this condition. This finding is more than minor because it was associated with a degraded condition thatcould concurrently influence mitigation equipment. Specifically, with the degraded flood barrier for the EDG building carbon dioxide suppression room, the ESW system booster pumps and return valves and the HPSW system return valves would be challenged to perform their safety function under design basis flood conditions. The NRC IMC 0609, Appendix G, "Shutdown Operations SDP," applies because the plant would be shutdown, at 112', in accordance with plant procedures, before flooding of EDG building would begin to occur at the 128' elevation, as noted in the LER. Also, as noted in the LER, the design basis flood would be expected to reach the 132' elevation. A Phase 1 SDP was performed using Checklist 5 of IMC 0609, Appendix G, Attachment 1. The inspectors determined that a Phase 2 or 3 SDP was required because the finding:*Increased the likelihood that a loss of decay heat removal will occur due to afailure of its support systems; *Would degrade the ability to cope with a loss of offsite power; and  
filling station, which is located outside the EDG building. The catch basin discharge was
*Would degrade the ability to establish an alternate core cooling path if decay heatremoval cannot be re-established for 24 hours. The inspectors determined that the finding was of very low safety significance (Green)because of:  the very low likelihood of occurrence of a design basis flood reaching the 132' elevation; flood alarms in the EDG building carbon dioxide suppression room that would enable operators to take actions to stop the flooding; or operators could manually operate the service water system return valves. A regional senior resident analyst reviewed and concurred with the inspectors risk assessment. This licensee-identified finding regarding the installation of a modification that placed the station in an unanalyzed condition involved a violation of 10 CFR 50.59. The enforcement aspects of this violation are discussed in Section
tied into the EDG building's oily waste separator tank, upstream of the flood protection
{{a|4OA7}}
isolation valve. This constituted an unanalyzed condition that degraded plant safety. In
==4OA7 of this report.==
the event of a design basis flood, a potential pathway existed for flood water to enter the
 
building through the floor drains. It was determined that the maximum credible flow rate
23Enclosure4OA5Other ActivitiesAs a plant status activity, the inspectors used guidance in NRC IP 60855.1, "Operation ofan Independent Spent Fuel Storage Installation at Operating Plants," to selectively verify that PBAPS performed dry cask loading in a safe manner and in compliance with approved procedures and work order instructions.4OA6Meetings, Including Exit.1Exit Meeting SummaryOn July 20, 2007, the resident inspectors presented the inspection results to Mr. J. Grimes and other PBAPS staff, who acknowledged the findings. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary. No proprietary information was identified.
would have exceeded the capability of the floor drain sump and sump pumps. Under
 
design basis flood conditions, the
===.2 Annual Assessment MeetingOn April 4, 2007, Mr. Paul Krohn, Mr. Mel Gray, the resident inspection staff, and otherNRC staff held a public meeting with Mr. Joe Grimes and other PBAPS staff, to discuss===
: [[ESW]] [[system booster pumps and return valves, and the]]
 
: [[HP]] [[]]
the results of the NRC's assessment of performance at PBAPS for the period January 1, 2006 through December 31, 2006. The handouts from the meeting are available electronically from the NRC's document system (ADAMS) under accession number ML071000066. Following the meeting, the NRC staff held a session to accept public comments and respond to public questions.4OA7Licensee-Identified ViolationsThe following violations of very low safety significance (Green) were identified by thelicensee and are violations of NRC requirements which meet the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as NCVs.*10 CFR 50.54(q) requires that the licensee shall follow and maintain in effectemergency plans which meet the standards in 50.47(b) and the requirements in Appendix E. The Exelon Nuclear Standardized Radiological Emergency Plan forPeach Bottom, Part II, Section E.2 b.1 states for State/Local Agencies: A notification shall be made within fifteen
SW system return valves would be challenged to perform their safety function.
: (15) minutes of the initial emergency classification. Contrary to this, on February 27, 2007, during an emergency event, Peach Bottom personnel failed to notify one local county within 15 minutes of an initial emergency declaration (Unusual Event); the notifications were completed in 18 minutes. The notification was not made in a timely manner because the primary phone link to the county was not available. Plant procedures require the notifications to be made using a backup phone. This finding is of very low safety significance (Green) because the notification was late by only 3 minutes, backup communication equipment was available, and procedures were available to use the backup communication equipment. This was entered in PBAPS's CAP as IR
Corrective actions recommended for this issue were documented in IR 554800 and
 
included revision of the applicable special event procedure for floods to mitigate this
condition. This finding is more than minor because it was associated with a degraded condition thatcould concurrently influence mitigation equipment. Specifically, with the degraded flood
barrier for the
: [[EDG]] [[building carbon dioxide suppression room, the]]
ESW system booster
pumps and return valves and the
: [[HP]] [[]]
SW system return valves would be challenged to
perform their safety function under design basis flood conditions. The
: [[NRC]] [[]]
IMC 0609,
Appendix G, "Shutdown Operations SDP," applies because the plant would be shutdown,
at 112', in accordance with plant procedures, before flooding of EDG building would begin
to occur at the 128' elevation, as noted in the
: [[LER.]] [[Also, as noted in the]]
LER, the design
basis flood would be expected to reach the 132' elevation. A Phase 1 SDP was
performed using Checklist 5 of IMC 0609, Appendix G, Attachment 1. The inspectors
determined that a Phase 2 or 3 SDP was required because the finding:*Increased the likelihood that a loss of decay heat removal will occur due to afailure of its support systems; *Would degrade the ability to cope with a loss of offsite power; and  
*Would degrade the ability to establish an alternate core cooling path if decay heatremoval cannot be re-established for 24 hours. The inspectors determined that the finding was of very low safety significance (Green)because of:  the very low likelihood of occurrence of a design basis flood reaching the
2' elevation; flood alarms in the EDG building carbon dioxide suppression room that
would enable operators to take actions to stop the flooding; or operators could manually
operate the service water system return valves. A regional senior resident analyst
reviewed and concurred with the inspectors risk assessment. This licensee-identified
finding regarding the installation of a modification that placed the station in an unanalyzed
condition involved a violation of 10 CFR 50.59. The enforcement aspects of this violation
are discussed in Section 4OA7 of this report.
23Enclosure4OA5Other ActivitiesAs a plant status activity, the inspectors used guidance in
: [[NRC]] [[]]
IP 60855.1, "Operation ofan Independent Spent Fuel Storage Installation at Operating Plants," to selectively verify
that
: [[PBA]] [[]]
PS performed dry cask loading in a safe manner and in compliance with
approved procedures and work order instructions.4OA6Meetings, Including Exit.1Exit Meeting SummaryOn July 20, 2007, the resident inspectors presented the inspection results to Mr.
: [[J.]] [[Grimes and other]]
PBAPS staff, who acknowledged the findings. The inspectors
asked the licensee whether any of the material examined during the inspection should be
considered proprietary. No proprietary information was identified. .2Annual Assessment MeetingOn April 4, 2007, Mr. Paul Krohn, Mr. Mel Gray, the resident inspection staff, and otherNRC staff held a public meeting with Mr. Joe Grimes and other
: [[PBA]] [[]]
PS staff, to discuss
the results of the
: [[NRC]] [['s assessment of performance at]]
PBAPS for the period January 1,
2006 through December 31, 2006. The handouts from the meeting are available
electronically from the
: [[NRC]] [['s document system (]]
: [[ADAMS]] [[) under accession number]]
: [[ML]] [[071000066. Following the meeting, the]]
NRC staff held a session to accept public
comments and respond to public questions.4OA7Licensee-Identified ViolationsThe following violations of very low safety significance (Green) were identified by thelicensee and are violations of
: [[NRC]] [[requirements which meet the criteria of Section]]
VI of
the
: [[NRC]] [[Enforcement Policy,]]
: [[NUREG]] [[-1600, for being dispositioned as]]
: [[NCV]] [[s.*10]]
CFR 50.54(q) requires that the licensee shall follow and maintain in effectemergency plans which meet the standards in 50.47(b) and the requirements in
Appendix
: [[E.]] [[The Exelon Nuclear Standardized Radiological Emergency Plan forPeach Bottom, Part]]
II, Section E.2 b.1 states for State/Local Agencies: A
notification shall be made within fifteen (15) minutes of the initial emergency
classification. Contrary to this, on February 27, 2007, during an emergency event,
Peach Bottom personnel failed to notify one local county within 15 minutes of an
initial emergency declaration (Unusual Event); the notifications were completed in
minutes. The notification was not made in a timely manner because the
primary phone link to the county was not available. Plant procedures require the
notifications to be made using a backup phone. This finding is of very low safety
significance (Green) because the notification was late by only 3 minutes, backup
communication equipment was available, and procedures were available to use
the backup communication equipment. This was entered in
: [[PBAPS]] [['s]]
CAP as IR
596641.
596641.
24Enclosure*10 CFR 50.59, "Changes, Tests, and Experiments," requires, in part, that thelicensee may make changes in the facility as described in the safety analysis
 
report without prior Commission approval, unless the proposed change involves a
24Enclosure*10 CFR 50.59, "Changes, Tests, and Experiments," requires, in part, that thelicensee may make changes in the facility as described in the safety analysis report without prior Commission approval, unless the proposed change involves a change in the TSs incorporated in the license or an unreviewed safety question (USQ). A proposed change shall be deemed to involve a USQ, in part, if the consequences of an accident or a malfunction of equipment important to safety previously evaluated in the safety analysis report may be increased. Contrary to this, in 1985, a change to the facility was made that remained in place until November 2006, without analyzing whether a USQ existed. Specifically, as documented in Section 4OA3.5, a plant modification performed in 1985 introduced a potential flood vulnerability for the EDG building carbon dioxide suppression room. The flood vulnerability posed by this change constituted an unanalyzed condition that degraded plant safety. This was identified in PBAPS's CAP as IR 554800. This finding is of very low safety significance (Green) because the likelihood of a design basis flood that could affect mitigation equipment is very small and manual operator action could be taken to mitigate the effects of a design basis flood.*TS 3.5.1, "Emergency Core Cooling Systems," requires that the ADS function offive SRVs be operable. TS 3.5.1, Action H, requires the plant to be brought to Mode 3 in 12 hours if two or more SRVs are inoperable. Contrary to the above, on September 28, 2006, the pneumatic actuation controls for the ADS function of two SRVs (71B and 71G) did not meet their allowable leak rate acceptance criteria.
change in the TSs incorporated in the license or an unreviewed safety question
 
(USQ). A proposed change shall be deemed to involve a USQ, in part, if the
Specifically, the as-found leak rates for the 71B and 71G SRVs were documented as off-scale and were in excess of the allowable the leak rate limit of 100 cc/min.
consequences of an accident or a malfunction of equipment important to safety
 
previously evaluated in the safety analysis report may be increased. Contrary to
this, in 1985, a change to the facility was made that remained in place until
November 2006, without analyzing whether a USQ existed. Specifically, as
documented in Section 4OA3.5, a plant modification performed in 1985 introduced
a potential flood vulnerability for the EDG building carbon dioxide suppression
room. The flood vulnerability posed by this change constituted an unanalyzed
condition that degraded plant safety. This was identified in
: [[PBAPS]] [['s]]
CAP as
IR 554800. This finding is of very low safety significance (Green) because the
likelihood of a design basis flood that could affect mitigation equipment is very
small and manual operator action could be taken to mitigate the effects of a design
basis flood.*TS 3.5.1, "Emergency Core Cooling Systems," requires that the
: [[ADS]] [[function offive]]
SRVs be operable. TS 3.5.1, Action H, requires the plant to be brought to
Mode 3 in 12 hours if two or more SRVs are inoperable. Contrary to the above, on
September 28, 2006, the pneumatic actuation controls for the ADS function of two
SRVs (71B and 71G) did not meet their allowable leak rate acceptance criteria.
Specifically, the as-found leak rates for the 71B and 71G SRVs were documented
as off-scale and were in excess of the allowable the leak rate limit of 100 cc/min.
Unit 2 was shutdown and in a refueling outage when the event was discovered.
Unit 2 was shutdown and in a refueling outage when the event was discovered.
However, Unit 2 had been operating for the previous 367 days. This issue was
 
entered in
However, Unit 2 had been operating for the previous 367 days. This issue was entered in PBAPS's CAP as IR 539277. As documented in Section 4OA3.4, a Phase 2 SDP determined that the finding was of very low safety significance (Green) because the success criteria for depressurization, on each of the applicable SDP notebook worksheets, only required the use of 2 of 11 SRVs.ATTACHMENT:  
: [[PBAPS]] [['s]]
 
: [[CAP]] [[as]]
=SUPPLEMENTAL INFORMATION=
: [[IR]] [[539277. As documented in Section 4]]
 
OA3.4, a
==KEY POINTS OF CONTACT==
Phase 2 SDP determined that the finding was of very low safety significance
Exelon Generation Company Personnel
(Green) because the success criteria for depressurization, on each of the
: [[contact::J. Grimes]], Site Vice President
applicable
: [[contact::M. Massaro]], Plant Manager
: [[SDP]] [[notebook worksheets, only required the use of 2 of 11]]
: [[contact::N. Alexakos]], Manager, Engineering-Programs
: [[SRV]] [[s.ATTACHMENT:]]
: [[contact::J. Armstrong]], Regulatory Assurance Manager
: [[SUPPLE]] [[]]
: [[contact::C. Behrend]], Engineering Director
: [[MENTAL]] [[]]
: [[contact::G. Jardel]], Manager, Emergency Preparedness
: [[INFORM]] [[]]
: [[contact::C. Jordan]], Chemistry Manager
: [[ATION]] [[A-1AttachmentSUPPLEMENTAL]]
: [[contact::D. Lewis]], Operations Director
: [[INFORM]] [[]]
: [[contact::H. McCrory]], Radiation Protection Technical Support Manager
: [[ATIONK]] [[EY]]
: [[contact::M. Ross]], Radwaste, Environmental Supervisor
: [[POINTS]] [[]]
: [[contact::G. Stathes]], Maintenance Director
: [[OF]] [[]]
: [[contact::S. Taylor]], Manager, Radiation Protection
: [[CONTAC]] [[]]
: [[contact::T. Van Wyen]], Operations Training Manager
TExelon Generation Company PersonnelJ. Grimes, Site Vice PresidentM. Massaro, Plant Manager
: [[contact::A. Wasong]], Training Director
N. Alexakos, Manager, Engineering-Programs
===NRC Personnel===
J. Armstrong, Regulatory Assurance Manager
: [[contact::F. Bower]], Senior Resident Inspector
C. Behrend, Engineering Director
: [[contact::M. Brown]], Resident Inspector
G. Jardel, Manager, Emergency Preparedness
: [[contact::R. Fuhrmeister]], Senior Project Engineer  
C. Jordan, Chemistry Manager
: [[contact::R. Nimitz]], Senior Health Physicist
D. Lewis, Operations Director
: [[contact::N. Perry]], Sr. Emergency Response Coordinator
H. McCrory, Radiation Protection Technical Support Manager
: [[contact::R. Cureton]], Emergency Preparedness Inspector
M. Ross, Radwaste, Environmental Supervisor
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
G. Stathes, Maintenance Director
Opened None.Opened and
S. Taylor, Manager, Radiation Protection
===Closed===
: [[T.]] [[Van Wyen, Operations Training Manager]]
: [[Closes finding::05000278/FIN-2007003-01]]FINInadequate Implementation of WOInstructions Caused the Installation of
: [[A.]] [[Wasong, Training Director]]
an Incorrect Size Breaker and
NRC PersonnelF. Bower, Senior Resident InspectorM. Brown, Resident Inspector
: Resulted in a Fire in the '4T4' 480 Volt
R. Fuhrmeister, Senior Project Engineer
: Load Center (Section 4OA3.1)05000277, 278/2007003-02NCVMissed Procedure Step Resulted inUnplanned Overloading of the E-3
R. Nimitz, Senior Health Physicist
: EDG (Section 4OA3.2)
: [[N.]] [[Perry, Sr. Emergency Response Coordinator]]
: A-2Attachment05000277, 278/2007003-03NCVInadequate Procedure AdherenceResults in Damage to the DDFP
: [[R.]] [[Cureton, Emergency Preparedness Inspector]]
(Section 4OA3.3)
: [[LIST]] [[]]
 
: [[OF]] [[]]
===Closed===
: [[ITEMS]] [[]]
: [[Closes finding::05000278/FIN-2007003-01]]FINInadequate Implementation of WOInstructions Caused the Installation of
: [[OPENED]] [[,]]
: [[CLOSED]] [[,]]
: [[AND]] [[]]
DISCUSSEDOpenedNone.Opened and Closed05000278/2007003-01FINInadequate Implementation of WOInstructions Caused the Installation of
an Incorrect Size Breaker and
an Incorrect Size Breaker and
Resulted in a Fire in the '4T4' 480 Volt
: Resulted in a Fire in the '4T4' 480 Volt
Load Center (Section
: Load Center (Section 4OA3.1)05000277, 278/2007003-02NCVMissed Procedure Step Resulted inUnplanned Overloading of the E-3
: [[4OA]] [[3.1)05000277, 278/2007003-02]]
: EDG (Section 4OA3.2)  
: [[NCVM]] [[issed Procedure Step Resulted inUnplanned Overloading of the E-3]]
: A-2Attachment05000277, 278/2007003-03NCVInadequate Procedure AdherenceResults in Damage to the DDFP
: [[EDG]] [[(Section 4]]
(Section 4OA3.3)
OA3.2)
 
A-2Attachment05000277, 278/2007003-03NCVInadequate Procedure AdherenceResults in Damage to the
===Discussed===
: [[DD]] [[]]
None.
: [[FP]] [[(Section]]
==LIST OF DOCUMENTS REVIEWED==
: [[4OA]] [[3.3)Closed05000277/2007002-04]]
==Section 1R01: Adverse WeatherWC-AA-107, Revision 4, Seasonal ReadinessOP-AA-108-111-1001, Revision 2, Severe Weather and Natural Disaster Guidelines==
URIIncorrect Size Breaker Resulted in aFire in the '4T4' 480 Volt Load Center
: OP-PB-108-111-1001, Revision 3, Preparation for Severe Weather
(Section
: RT-O-040-610-2, Revision 12, Outbuilding HVAC and Equipment Inspection for SummerOperationSO 52A.1.B, Revision 39, Diesel Generator Operations
: [[4OA]] [[3.1)05000277/2007002-05]]
 
: [[URI]] [[Missed Procedure Step Resulted inUnplanned Overloading of the E-3]]
==Section 1R04: Equipment AlignmentCOL 52A.1.A-3, Revision 12,==
: [[EDG]] [[(Section 4]]
: E-3 Diesel Generator Normal StandbySO 53.7.A - App 1, Revision 0, Removal of 220-08 Line from Service
: [[OA]] [[3.2)05000277/2006002-00LERADS]]
: COL 13.1.A-2, Revision 19, RCIC System
: [[SRV]] [[Deficiencies(Section 4]]
: COL 33.1.A-2, Revision 20, ESW System (Unit 2 and Common)
: [[OA]] [[3.4)05000277/2006004-00]]
: COL 32.1.A-2, Revision 10, HPSW System
: [[LE]] [[]]
: SO 32.1.A-2, Revision 12, HPSW System Startup and Normal Operatoins  
RPlant Modification Created DieselGenerator Building Carbon Dioxide
: A-3AttachmentP&ID DiagramM-315 Sheet 1, Revision 64, ESW and HPSW SystemsM-315 Sheet 4, Revision 53, ESW and HPSW Systems
Suppression Room Flooding
: M-315, Sheet 1, Revision 65, ESW and HPSWSystemsM-330, Sheet 1, Revision 35, Emergency Cooling System
Vulnerability (Section
: M-361, Sheet1, Revision 80, RHR System
: [[4OA]] [[3.5)DiscussedNone.]]
: M-361, Sheet 2, Revision 67, RHR System
: [[LIST]] [[]]
 
: [[OF]] [[]]
==Section 1R05: Fire ProtectionPF-63, Revision 1, Prefire Strategy Plan Unit 3 Reactor Bldg.==
: [[DOCUME]] [[NTS]]
: RCIC Room, 88' ElevationPF-70, Revision 2, Prefire Strategy Plan Standby Gas Treatment Room, Radwaste Building,91' 6" ElevationPF-13H, Revision 3, Prefire Strategy Plan North CRS Equipment and West Corridor, Unit 3Reactor Building, 135' ElevationPF-55, Revision 3, Prefire Strategy Plan, Fire Zone 55, Unit 3 Refuel Floor, Reactor Building,234' ElevationPF-13D, Revision 1, Prefire Strategy Plan 3 'A' & 3 'C' Core Spray Rooms, Reactor Building,91'6" Elevation, Fire Zones 13D & 13EPF-60, Revision 1, Prefire Strategy Plan, Unit 2 Reactor Building RCIC Room, 88' Elevation
: [[REVIEW]] [[]]
: PF-127, Revision 4, Prefire Strategy Plan, Unit 2 Emergency Battery/ Switchgear Room andRadwaste Corridor,
: [[EDS]] [[ection 1R01: Adverse WeatherWC-AA-107, Revision 4, Seasonal ReadinessOP-AA-108-111-1001, Revision 2, Severe Weather and Natural Disaster Guidelines]]
: TB-135PF-132, Revision 4, Prefire Strategy Plan, Diesel Generator Building, Elevation 127', Fire Zone 132PF-151, Revision 3, Prefire Strategy Plan, Unit 2 Main Transformer Yard, Fire Zone 151
: [[OP]] [[-]]
: PF-164, Revision 0, Prefire Strategy Plan, 2 Startup Switchgear Building, Fire Zone 164
: [[PB]] [[-108-111-1001, Revision 3, Preparation for Severe Weather]]
 
: [[RT]] [[-O-040-610-2, Revision 12, Outbuilding]]
==Section 1R12: Maintenance EffectivenessIR
: [[HVAC]] [[and Equipment Inspection for SummerOperationSO]]
: 607398, Functional Failure of 3AE015 During '4T4' Breaker FireIR
: [[52A.]] [[1.B, Revision 39, Diesel Generator OperationsSection 1R04: Equipment Alignment]]
: 596616, Fault at Unit 3 'B' Iso-Phase Cooler Fan Breaker in 4T4==
: [[COL]] [[]]
: IR 614945, Potential Extent of Condition Concern for MCC Bucket Stabs
: [[52A.]] [[1.A-3, Revision 12, E-3 Diesel Generator Normal Standby]]
: IR 619579, 480 V Breaker Interference Angle Location Incorrect
: [[SO]] [[53.7.A - App 1, Revision 0, Removal of 220-08 Line from Service]]
: IR 617890, Conflicting Data on Cubicle Size of 2 'A' EHC Pump Breaker
: [[COL]] [[13.1.A-2, Revision 19,]]
: IR 599184, Extent of Condition Walkdown of Unit 2 480 V Load Center Bus
: [[RCIC]] [[System]]
: IR 606397, Perform ITE Rejection Tab Walkdown
: [[COL]] [[33.1.A-2, Revision 20,]]
: IR 599203, Extent of Condition Walkdown of Unit 3 480 V Load Center Bus
: [[ESW]] [[System (Unit 2 and Common)]]
: IR 599208, Extent of Condition Walkdown of Common 480 V Load Center Bus
: [[COL]] [[32.1.A-2, Revision 10,]]
: IR 634973, ITE Breaker Found With No Rejection Tab
: [[HPSW]] [[System]]
: IR 634971, ITE Breaker Found With No Rejection Tab
: [[SO]] [[32.1.A-2, Revision 12,]]
: IR 634962, ITE Breaker Found With No Rejection Tab
HPSW System Startup and Normal Operatoins
: IR 634964, ITE Breaker Found With No Rejection Tab
A-3AttachmentP&ID DiagramM-315 Sheet 1, Revision 64,
: IR 634966, ITE Breaker Found With No Rejection Tab
: [[ESW]] [[and]]
: IR 634965, ITE Breaker Found With No Rejection Tab
: [[HPSW]] [[SystemsM-315 Sheet 4, Revision 53,]]
: IR 600797, 2007 Buried Pipe Program Inspections
: [[ESW]] [[and]]
: IR 623638, EOC: Generate PM per PCM Template Requirements
HPSW Systems
: IR 623646, EOC: Generate PM per PCM Template Requirements  
M-315, Sheet 1, Revision 65,
: A-4AttachmentIR
: [[ESW]] [[and]]
: 623635, EOC: Generate PM per PCM Template RequirementsIR
HPSWSystemsM-330, Sheet 1, Revision 35, Emergency Cooling System
: 603279, Inspect and Clean ESW X-Tie Piping (HV-512A-B) WW 0730
M-361, Sheet1, Revision 80, RHR System
: IR 632688, 2 'A' EHC PP Breaker Cubicle Frame Size Incorrect
M-361, Sheet 2, Revision 67,
: IR 589654, Potential For Silt Buildup in the ESW Pump Crosstie Piping
: [[RHR]] [[SystemSection 1R05: Fire Protection]]
: ACPS 07-0-002,
: [[PF]] [[-63, Revision 1, Prefire Strategy Plan Unit 3 Reactor Bldg.]]
: HV-0-33-512A, A ESW Pump Discharge Loop X-tie
: [[RCIC]] [[Room, 88' Elevation]]
: ST-O-033-300-2, Revision 31, ESW, Valve, Unit Cooler and ECT Functional Inservice Test
: [[PF]] [[-70, Revision 2, Prefire Strategy Plan Standby Gas Treatment Room, Radwaste Building,91' 6" ElevationPF-13H, Revision 3, Prefire Strategy Plan North]]
: ACPS 07-0-002,
: [[CRS]] [[Equipment and West Corridor, Unit 3Reactor Building, 135' Elevation]]
: HV-0-33-512A, A ESW Pump Discharge Loop X-tie
: [[PF]] [[-55, Revision 3, Prefire Strategy Plan, Fire Zone 55, Unit 3 Refuel Floor, Reactor Building,234' ElevationPF-13D, Revision 1, Prefire Strategy Plan 3 'A' & 3 'C' Core Spray Rooms, Reactor Building,91'6" Elevation, Fire Zones 13D &]]
: ST-O-033-300-2, Revision 31, ESW, Valve, Unit Cooler and ECT Functional Inservice Test Performance Monitoring - Unavailability - System 33 (ESW) - Jun 2005 -> Jun 2007
: [[13EPF]] [[-60, Revision 1, Prefire Strategy Plan, Unit 2 Reactor Building]]
: Clearance
: [[RCIC]] [[Room, 88' Elevation]]
: 07000529, Emergency Cooling Water Pump Discharge Valve
: [[PF]] [[-127, Revision 4, Prefire Strategy Plan, Unit 2 Emergency Battery/ Switchgear Room andRadwaste Corridor,]]
: ER-AA-5400, Revision 0, Buried Piping and Raw Water Corrosion Program Guide
: [[TB]] [[-135PF-132, Revision 4, Prefire Strategy Plan, Diesel Generator Building, Elevation 127', FireZone 132PF-151, Revision 3, Prefire Strategy Plan, Unit 2 Main Transformer Yard, Fire Zone 151]]
: ER-AA-5300, Revision 0, Raw Water Corrosion Program Guide
: [[PF]] [[-164, Revision 0, Prefire Strategy Plan, 2 Startup Switchgear Building, Fire Zone 164Section 1R12: Maintenance Effectiveness]]
: ER-AA-5400-1002, Revision 0, Buried Piping Examination GuideSection 1R13: Maintenance Risk Assessments and Emergent Work ControlWC-AA-101, "On-line Work Control Process"Adverse Condition Monitoring and Contingency Plan (CAMP), 3 'A' Recirculation Pump Seal Unstable Second Stage Seal Temperature and Increasing Second Stage Seal Pressure, Dated 04/17/2007AR A1612541, Rising 3 'A' Recirculation Pump #2 Seal Temperature
: [[IR]] [[607398, Functional Failure of]]
: AR A1610537, High Lube Oil Temperature Alarm During E-2 EDG Run
: [[3AE]] [[015 During '4T4' Breaker Fire]]
: AR A1613094-01, Technical Evaluation: CRD Suction Source Swap from Condensate to Unit 3 CSTIR
: [[IR]] [[596616, Fault at Unit 3 'B' Iso-Phase Cooler Fan Breaker in 4T4]]
: 623723, Bolt and Heli-coil Found Damaged at Disassembly on 00T634
: [[IR]] [[614945, Potential Extent of Condition Concern for]]
: SF-220, Revision 21, Spent Fuel Cask Loading and Transport Operations
MCC Bucket Stabs
: A1406063, Review of Mod 79-028 Recirculation Seal Pressure Bleed Off
: [[IR]] [[619579, 480 V Breaker Interference Angle Location Incorrect]]
: EC 360901, Exelon Fleet Reactor Recirculation Pump Seal Condition Monitoring TemplateIR
: [[IR]] [[617890, Conflicting Data on Cubicle Size of 2 'A']]
: 620785, Continuous Venting of the Recirculation Seals not EvaluatedAO 2A.16-3, Revision 2, Manual Adjustment of Recirculation Pump Seal Second Stage PressureSO 2A.1.C-3, Revision 10, Operation of the Recirculation Pump Seal Purge System
EHC Pump Breaker
: A1439223, 3AP034: Seal Hi Temp Alarm & Hi 2
: [[IR]] [[599184, Extent of Condition Walkdown of Unit 2 480 V Load Center Bus]]
nd Stage PressureACMP - Unit 3, 3 'B' Recirculation Pump Seal Increasing Second Stage Seal Pressure
: [[IR]] [[606397, Perform]]
: A1613202, 3 'B' Recirculation Pump 2
ITE Rejection Tab Walkdown
nd Stage Seal PressureIR
IR 599203, Extent of Condition Walkdown of Unit 3 480 V Load Center Bus
: 619609, 3 'B' Recirculation Pump 2
: [[IR]] [[599208, Extent of Condition Walkdown of Common 480 V Load Center Bus]]
nd Stage Seal PressureARC 30C204M A-1, Revision 4 - A Recirculation Pump Seal Stage 2 Hi Flow
: [[IR]] [[634973,]]
: ARC 30C204M A-2, Revision 6 - A Recirculation Pump Seal Stage 2 Lo Flow
: [[ITE]] [[Breaker Found With No Rejection Tab]]
: OP-PB-108-101-1002, "Guidelines for Control of Protected Equipment," Revision 4
: [[IR]] [[634971,]]
: WC-AA-101, "On-Line Work Control Process," Revision 13
: [[ITE]] [[Breaker Found With No Rejection Tab]]
: IR 626534, Equipment Not Protected as Required.
: [[IR]] [[634962,]]
: IR 624653, Protected Equipment List for 2SUE Outage Incomplete
: [[ITE]] [[Breaker Found With No Rejection Tab]]
: IR 617946, Protected Equipment List Issued 4/16/07 Initially Incomplete
: [[IR]] [[634964,]]
: IR 504032, Exaggerated Paragon List of Protected Equipment
: [[ITE]] [[Breaker Found With No Rejection Tab]]
: IR 462364-18-04, Paragon Refresher Training
: [[IR]] [[634966,]]
: IR 624599, U3 RHR Pump Testing Not Performed per Schedule
: [[ITE]] [[Breaker Found With No Rejection Tab]]
: IR 634657, PRA Support for Protecting Equipment
: [[IR]] [[634965,]]
: IR 474569-17-08, Develop a Tutorial that Help Crews with Paragon
ITE Breaker Found With No Rejection Tab
: IR 624599, U3 RHR Pump Testing Not Performed per Schedule
: [[IR]] [[600797, 2007 Buried Pipe Program Inspections]]
: IR 644648, Inadequate Guidance in
: [[IR]] [[623638,]]
: WC-AA-101 for Protecting Equipment  
: [[EOC]] [[: Generate]]
: A-5AttachmentARC-216 20C212L D-1, Revision 5, C Air Comp TroubleSO 36A.7.A-2, Revision 3, Unit 2 'C' Air Compressor Shutdown
: [[PM]] [[per]]
: ON-119, Revision 14, Loss of Instrument Air
: [[PCM]] [[Template Requirements]]
: ARC-216 20C212L D-2, Revision 2 Service Air Header Lo Press
: [[IR]] [[623646,]]
: ARC-316 20C212L D-2, Revision 1, Service Air Header Lo Press
: [[EOC]] [[: Generate]]
: R1032642, 3CK001 - PM: Perform Annual PM on Compressor
: [[PM]] [[per]]
: SO 36A.1.A-2, Revision 2, Unit 2 'C' Air Compressor Return-to-Service and Service Air Systems Return to Normal OperationIR
PCM Template Requirements
: 642127, Critique IR on Loss of Service Air to Unit 2 and Unit 3DrawingsP&I Diagram M-356, CRD Rod Drive Hydraulic System Part A, Sheet 2P&I Diagram M-353, Reactor Recirculation Pump System
A-4AttachmentIR 623635,
 
: [[EOC]] [[: Generate]]
==Section 1R15: Operability EvaluationsIR 615433,==
: [[PM]] [[per]]
: E-4 EDG - 10
: [[PCM]] [[Template Requirements]]
: CFR 21 Notification for Cam Roller Bushing Material Issue Fairbanks Morse Engine Notification Report Serial Number 06-04, 10
: [[IR]] [[603279, Inspect and Clean]]
: CFR 21 Notification, CamRoller Bushing Incorrect Material, dated April 9, 2007Event Notification Number 43294, Part 21 Notification - Diesel Cam Roller Bushing Failures
: [[ESW]] [[X-Tie Piping (]]
: IR 388397-04, Prompt Investigation of 3 'A' RRP #2 Seal Cavity Temperature HighAdverse Condition Monitoring and Contingency Plan (CAMP), 3 'A' RRP Unstable Second Stage Seal Temperature and Increasing Second Stage Seal Pressure, dated 04/17/2007Operational and Technical Decision Making (OTDM) No. 07-01, 3 'A' RRP Seal Issues, dated04/17/2007Abnormal Operations (AO) procedure 2A.16-3, Manual Adjustment Recirculation Pump SealSecond Stage PressureOTDM No. 07-02, 3 'A' RRP Seal Temperatures - Re-align CRD Suction Source fromCondensate System to U3 CST, dated 04/20/2007AR A1613094-01, Technical Evaluation:
: [[HV]] [[-512A-B) WW 0730]]
: CRD Suction Source Swap from Condensate to Unit 3 CST PBAPS Technical Requirements Log, Item Number 07-3-080, PTRM 3.6, Function 7, MainSteam Relief Valves, dated May 17, 2007Adverse Condition Monitoring Plan:
: [[IR]] [[632688, 2 'A']]
: DPT-2-02-117DH Sensing Line Leakage, datedMay 24, 2007A1615458, Small Leak on
: [[EHC]] [[PP Breaker Cubicle Frame Size Incorrect]]
: DPT-2-02-117D Line Snubber Threaded Cap
: [[IR]] [[589654, Potential For Silt Buildup in the]]
: C0221439, Replace Snubber During an Outage
: [[ESW]] [[Pump Crosstie Piping]]
: PB
: [[ACPS]] [[07-0-002,]]
: ECR 03-00326 000, Revise Instrument Rack Drawings with a Note for Snubbers
: [[HV]] [[-0-33-512A, A ESW Pump Discharge Loop X-tie]]
 
: [[ST]] [[-O-033-300-2, Revision 31,]]
==Section 1R19: Post-Maintenance TestingAR A1610537, High Lube Oil Temperature Alarm During==
: [[ESW]] [[, Valve, Unit Cooler and ECT Functional Inservice Test]]
: E-2 EDG RunR1049367, Unit 3
: [[ACPS]] [[07-0-002,]]
: HCU 50-43: HCU Overhaul
: [[HV]] [[-0-33-512A, A ESW Pump Discharge Loop X-tie]]
: ST-R-003-480-3, Average Scram Times for ODYN/B Minimum Critical Power Ratio (MCPR) RequirementsC0216504,
: [[ST]] [[-O-033-300-2, Revision 31,]]
: PS-2-13-067-01: Replace Pressure Switch
ESW, Valve, Unit Cooler and ECT Functional Inservice Test
: ST-O-013-301-2, Revision 31, RCIC Pump, Valve, Flow and Unit Cooler Functional andInservice Test, Conducted on April 5, 2007  
Performance Monitoring - Unavailability - System 33 (ESW) - Jun 2005 -> Jun 2007
: A-6AttachmentC0215740, 2BG002, Replace EndbellMA-AA-716-230-1002, Revision 1, Vibration Analysis/ Acceptance Guideline
Clearance 07000529, Emergency Cooling Water Pump Discharge Valve
: MA-AA-716-230-1003, Revision 1, Thermography Program Guide
: [[ER]] [[-]]
: SO 60F.1.A-2, Revision 9, Reactor Protection System MG Set and Power Distribution System Startup from Dead Bus ConditionR0629147, 3R4-U-C (7033B), Perform MCU Inspection
: [[AA]] [[-5400, Revision 0, Buried Piping and Raw Water Corrosion Program Guide]]
: A1619582, 3CP343: Pump/Motor Found Seized during Breaker PMT
: [[ER]] [[-]]
: IR 638369, 3C Glycol Pump found seized during breaker PMT
: [[AA]] [[-5300, Revision 0, Raw Water Corrosion Program Guide]]
: SO 8G.6.A-3, Revision 3, Placing a Standby Off-Gas Glycol Pump in Service and Placing the InService Pump in Standby or Off
: [[ER]] [[-]]
 
AA-5400-1002, Revision 0, Buried Piping Examination GuideSection 1R13: Maintenance Risk Assessments and Emergent Work ControlWC-AA-101, "On-line Work Control Process"Adverse Condition Monitoring and Contingency Plan (CAMP), 3 'A' Recirculation Pump Seal
==Section 1R22: Surveillance TestingS12T-MIS-8547-C1CQ, Revision 13, Calibration/Functional Check of Channel C Group 1, 4 and 5 of==
Unstable Second Stage Seal Temperature and Increasing Second Stage Seal Pressure, Dated 04/17/2007AR A1612541, Rising 3 'A' Recirculation Pump #2 Seal Temperature
: PCIV Logic for
: [[AR]] [[A1610537, High Lube Oil Temperature Alarm During E-2]]
: TSS-80547CST-R-003-485-3, CRD Scram Insertion Timing of Selected Control Rods, Revision 19, completed May 5, 1997
: [[EDG]] [[Run]]
 
: [[AR]] [[A1613094-01, Technical Evaluation:]]
==Section 1R23: Temporary Plant ModificationsIR
: [[CRD]] [[Suction Source Swap from Condensate to Unit]]
: 618478, Provide Supplemental Cooling to the 3 'A'==
: [[3 CST]] [[]]
: RR Seal Purge LineIR
IR 623723, Bolt and Heli-coil Found Damaged at Disassembly on 00T634
: 625092, Equipment Discovered on Floor Hatch H11 in Unit 3 Reactor Building
SF-220, Revision 21, Spent Fuel Cask Loading and Transport Operations
: WO
A1406063, Review of Mod 79-028 Recirculation Seal Pressure Bleed Off
: C0221034, TCCP 07-00172, Install Cooling Unit
: [[EC]] [[360901, Exelon Fleet Reactor Recirculation Pump Seal Condition Monitoring Template]]
: AR A1613094, Provide Supplemental Cooling to the 3 'A' RR Seal Purge Line
: [[IR]] [[620785, Continuous Venting of the Recirculation Seals not EvaluatedAO]]
: SP
: [[2A.]] [[16-3, Revision 2, Manual Adjustment of Recirculation Pump Seal Second Stage Pressure]]
: SO.005-3, Revision 1, Routine Inspection of the 3 'A' Recirculation Seal Purge SupplementalCooling System
SO 2A.1.C-3, Revision 10, Operation of the Recirculation Pump Seal Purge System
 
A1439223,
==Section 1EP2: Alert and Notification System (ANS) EvaluationPeach Bottom Nuclear Power Plant Upgraded Public Alert and Notification Report, April 2005FEMA==
: [[3AP]] [[034: Seal Hi Temp Alarm & Hi 2nd Stage Pressure]]
: ANS Design Report, December 2005EP-MA-121-1002 "Exelon East Alert and Notification System (ANS) Program," Revision 4
ACMP - Unit 3, 3 'B' Recirculation Pump Seal Increasing Second Stage Seal Pressure
: EP-MA-121-1004 "Exelon East ANS Corrective Maintenance," Revision 4
A1613202, 3 'B' Recirculation Pump 2nd Stage Seal PressureIR 619609, 3 'B' Recirculation Pump 2nd Stage Seal PressureARC 30C204M A-1, Revision 4 - A Recirculation Pump Seal Stage 2 Hi Flow
: EP-MA-121-1005 "Exelon East ANS Preventive Maintenance Program," Revision 3
: [[ARC]] [[30C204M A-2, Revision 6 - A Recirculation Pump Seal Stage 2 Lo Flow]]
: EP-MA-121-1006 "Exelon East ANS Siren Monitoring, Troubleshooting, and Testing," Revision 5Corrective Maintenance Field Work Instructions for ANS Control Points, Repeaters and Sirens, Approved December 2004Preventative Maintenance Field Work Instructions for ANS Control Points, Repeaters and SirensIRs:
: [[OP]] [[-]]
: 00433494 00565056
: [[PB]] [[-108-101-1002, "Guidelines for Control of Protected Equipment," Revision 4]]
: 00352078
: [[WC]] [[-]]
: 00597065
AA-101, "On-Line Work Control Process," Revision 13
: 00481763 00451040
: [[IR]] [[626534, Equipment Not Protected as Required.]]
: 00520830
: [[IR]] [[624653, Protected Equipment List for 2]]
: 00521321
SUE Outage Incomplete
: 00533157 00541478
IR 617946, Protected Equipment List Issued 4/16/07 Initially Incomplete
: 00596641  
IR 504032, Exaggerated Paragon List of Protected Equipment
: A-7Attachment
: [[IR]] [[462364-18-04, Paragon Refresher Training]]
 
: [[IR]] [[624599, U3]]
==Section 1EP4: Emergency Action Level (EAL) and Emergency Plan ChangesEP-AA-120-1001 "10==
: [[RHR]] [[Pump Testing Not Performed per Schedule]]
: CFR 50.54(q) Change Evaluation," Revision 406-12  "ERO Training and Qualification"
: [[IR]] [[634657,]]
: TQ-AA-113, Revision 7
PRA Support for Protecting Equipment
: 06-16  "Radiological Emergency Plan"
: [[IR]] [[474569-17-08, Develop a Tutorial that Help Crews with Paragon]]
: EP-AA-1000, Revision 17
: [[IR]] [[624599, U3]]
: 06-33  "EP Plan Administration"
: [[RHR]] [[Pump Testing Not Performed per Schedule]]
: EP-AA-120, Revision 7
: [[IR]] [[644648, Inadequate Guidance in]]
: 06-96  "Emergency Preparedness Advisory Committee"
WC-AA-101 for Protecting Equipment
: EP-AA-120-1004, Revision 0
A-5AttachmentARC-216 20C212L D-1, Revision 5, C Air Comp TroubleSO 36A.7.A-2, Revision 3, Unit 2 'C' Air Compressor Shutdown
: 06-97  "Quarterly Satellite Phone Test"
ON-119, Revision 14, Loss of Instrument Air
: EP-MA-124-1004, Revision 0
ARC-216 20C212L D-2, Revision 2 Service Air Header Lo Press
: 06-99  "EP Fundamentals"
ARC-316 20C212L D-2, Revision 1, Service Air Header Lo Press
: EP-AA-1101, Revision 3
R1032642,
: 06-101"Exelon East ANS Program"
: [[3CK]] [[001 -]]
: EP-MA-121-1002, Revision 4
: [[PM]] [[: Perform Annual PM on Compressor]]
: 06-102"Exelon East ANS Corrective Maintenance Program"
: [[SO]] [[36A.1.A-2, Revision 2, Unit 2 'C' Air Compressor Return-to-Service and Service Air Systems Return to Normal Operation]]
: EP-MA-121-1004, Revision 4
: [[IR]] [[642127, Critique]]
: 06-103"Exelon East ANS Preventative Maintenance Program"
: [[IR]] [[on Loss of Service Air to Unit 2 and Unit 3DrawingsP&I Diagram M-356,]]
: EP-MA-121-1005, Revision 3
: [[CRD]] [[Rod Drive Hydraulic System Part A, Sheet]]
: 06-108"ERO Fundamentals"
: [[2P&I]] [[Diagram M-353, Reactor Recirculation Pump SystemSection 1R15: Operability Evaluations]]
: EP-AA-1102, Revision 2
: [[IR]] [[615433, E-4]]
: 06-110"Mid-Atlantic ERO Notification or Augmentation" EP-AA-112-100-F-07
: [[EDG]] [[- 10]]
: 07-11"Exelon East ANS Siren Monitoring, Troubleshooting, and Testing"
: [[CFR]] [[21 Notification for Cam Roller Bushing Material Issue Fairbanks Morse Engine Notification Report Serial Number 06-04, 10 CFR 21 Notification, CamRoller Bushing Incorrect Material, dated April 9, 2007Event Notification Number 43294, Part 21 Notification - Diesel Cam Roller Bushing Failures]]
: EP-MA-121-1006, Revision 407-12"ANS Siren Monthly Test"
: [[IR]] [[388397-04, Prompt Investigation of 3 'A']]
: RT-E-101-901-2, Revision 8
RRP #2 Seal Cavity Temperature HighAdverse Condition Monitoring and Contingency Plan (CAMP), 3 'A' RRP Unstable Second
: 07-18"Radiological Emergency Plan Annex for PBAPS"
Stage Seal Temperature and Increasing Second Stage Seal Pressure, dated 04/17/2007Operational and Technical Decision Making (OTDM) No. 07-01, 3 'A'
: EP-AA-1007, Revision 14
: [[RRP]] [[Seal Issues, dated04/17/2007Abnormal Operations (]]
: 07-39"Exelon East ANS Siren Monitoring, Troubleshooting, and Testing"
: [[AO]] [[) procedure]]
: EP-MA-121-1006, Revision 5
: [[2A.]] [[16-3, Manual Adjustment Recirculation Pump SealSecond Stage Pressure]]
 
: [[OTDM]] [[No. 07-02, 3 'A']]
==Section 1EP5: Correction of Emergency Preparedness WeaknessesEP-AA-125 "Emergency Preparedness Self Evaluation Process," Revision4LS-AA-126 "Self-Assessment Program," Revision 5==
: [[RRP]] [[Seal Temperatures - Re-align]]
: LS-AA-126-1001 "Focused Area Self-Assessments," Revision 4
: [[CRD]] [[Suction Source fromCondensate System to U3]]
: Unusual Event Evaluation Reports dated 10/4/06, 11/21/06, 4/16/07
: [[CST]] [[, dated 04/20/2007]]
: ASSAs:
: [[AR]] [[A1613094-01, Technical Evaluation:]]
: 547869, 565747-04
: [[CRD]] [[Suction Source Swap from Condensate to Unit 3]]
: NOSA:-PEA-06-03 dated 4/13/06
: [[CST]] [[]]
: NOSA-PEA-07-04 dated 5/9/07  
: [[PBAPS]] [[Technical Requirements Log, Item Number 07-3-080,]]
: A-8AttachmentIRs:
: [[PTRM]] [[3.6, Function 7, MainSteam Relief Valves, dated May 17, 2007Adverse Condition Monitoring Plan:]]
: 00433494
: [[DPT]] [[-2-02-117]]
: 00565056
DH Sensing Line Leakage, datedMay 24, 2007A1615458, Small Leak on DPT-2-02-117D Line Snubber Threaded Cap
: 00352078
C0221439, Replace Snubber During an Outage
: 00481763
: [[PB]] [[]]
: 00451040 00520830
: [[ECR]] [[03-00326 000, Revise Instrument Rack Drawings with a Note for SnubbersSection 1R19: Post-Maintenance TestingAR A1610537, High Lube Oil Temperature Alarm During E-2]]
: 00533157
: [[EDG]] [[RunR1049367, Unit 3]]
: 00541478
: [[HCU]] [[50-43: HCU Overhaul]]
: 00596641 00597065
: [[ST]] [[-R-003-480-3, Average Scram Times for]]
: 00521321Section 1EP6: Drill EvaluationPeach Bottom Atomic Power Station, May 15, 2007, Off-Year Exercise, Drill ScenarioPeach Bottom Atomic Power Station May 15
: [[ODYN]] [[/B Minimum Critical Power Ratio (MCPR) RequirementsC0216504, PS-2-13-067-01: Replace Pressure Switch]]
th, 2007 Off-Year Exercise Report datedJune 14, 2007IR
: [[ST]] [[-O-013-301-2, Revision 31,]]
: 630584, Enhancement Opportunity from May 2007 EP Drill
RCIC Pump, Valve, Flow and Unit Cooler Functional andInservice Test, Conducted on April 5, 2007
: IR 629910, Late State\Local Notification Made During an EP Drill
A-6AttachmentC0215740,
: IR 629970, EAL Classification During Drill Not Timely Quick Human Performance Investigation Report, PB EAL Classification During Drill Not Timely, 05/15/07Quick Human Performance Investigation, Repetitive Issue With Not Completing State/Local Notifications on Time, 5/15/07 Section 2PS2 : Radioactive Material Processing and Transportation10 CFR Part 61 Sampling and Analysis Results (Waste Streams)Radioactive Material Shipping Documentation Radioactive Shipping Container Certifications Audit Template: Chemistry, Radwaste, Effluent and Environmental Monitoring Handling, Storage and Shipping Topical Report, Mobile In-container De-watering and Solidification System
: [[2BG]] [[002, Replace Endbell]]
: DOT-Type A, Test and Evaluation for Type A Packaging Waste Disposal Facility State Licenses Training Program - DOT/79-19 Training for Support of Radioactive and Asbestos Shipments Training Program - Site Specific Portion of Radioactive Material Shipping Training Program Training Program - Shipper Refresher Type B Cask Handling and Loading Procedures
: [[MA]] [[-AA-716-230-1002, Revision 1, Vibration Analysis/ Acceptance Guideline]]
: RT-W-020-980-2, Updating Radwaste Classification Computer Programs
: [[MA]] [[-]]
: RP-AA-605, 10
: [[AA]] [[-716-230-1003, Revision 1, Thermography Program Guide]]
: CFR 61 Compliance Program
: [[SO]] [[60F.1.A-2, Revision 9, Reactor Protection System]]
: RP-AA-605, 10
MG Set and Power Distribution System Startup from Dead Bus ConditionR0629147, 3R4-U-C (7033B), Perform MCU Inspection
: CFR 61 Program
A1619582,
: RP-PB-605-1001, Peach Bottom 10
: [[3CP]] [[343: Pump/Motor Found Seized during Breaker]]
: CFR 61 Sampling
: [[PMT]] [[]]
 
: [[IR]] [[638369, 3C Glycol Pump found seized during breaker]]
==Section 4OA1: Performance Indicator VerificationLS-AA-2001, Revision 6, Collecting and Reporting of==
: [[PMT]] [[]]
: NRC Performance Indicators DataLS-AA-2090, Revision 4, Monthly Data Elements for NRC RCS Specific Activity
: [[SO]] [[8G.6.A-3, Revision 3, Placing a Standby Off-Gas Glycol Pump in Service and Placing the InService Pump in Standby or OffSection 1R22: Surveillance TestingS12T-]]
: LS-AA-2100, Revision 5, Monthly Data Elements for NRC RCS Leakage
: [[MIS]] [[-8547-C1CQ, Revision 13, Calibration/Functional Check of Channel C Group 1, 4 and 5 of]]
: ST-O-020-560-2, Reactor Coolant Leakage Test (sample of completed test records)
: [[PCIV]] [[Logic for]]
: ST-O-020-560-3, Reactor Coolant Leakage Test (sample of completed test records)
: [[TSS]] [[-80547CST-R-003-485-3,]]
: ST-C-095-864-2, Off Gas Monitor Response and Release Rate Verification by a Grab Sample  
: [[CRD]] [[Scram Insertion Timing of Selected Control Rods, Revision 19, completed May 5, 1997Section 1R23: Temporary Plant Modifications]]
: A-9AttachmentST-C-095-864-3, Off Gas Monitor Response and Release Rate Verification by a Grab SampleST-C-095-820-2, Determination of Dose Equivalent µCi/g I-131 in Primary Coolant
: [[IR]] [[618478, Provide Supplemental Cooling to the 3 'A']]
: ST-C-095-820-3, Determination of Dose Equivalent µCi/g I-131 in Primary Coolant
: [[RR]] [[Seal Purge Line]]
: CH-407, Sampling of Reactor Water
: [[IR]] [[625092, Equipment Discovered on Floor Hatch H11 in Unit 3 Reactor Building]]
: CH-C-601, Determination of Dose Equivalent I-131
: [[WO]] [[C0221034,]]
: ERO Drill Participation PI data, April 2006 - March 2007
: [[TCCP]] [[07-00172, Install Cooling Unit]]
: Public Notification System PI data, April 2006 - March 2007
: [[AR]] [[A1613094, Provide Supplemental Cooling to the 3 'A']]
: DEP PI data, April 2006 - March 2007
: [[RR]] [[Seal Purge Line]]
 
: [[SP]] [[]]
==Section 4OA2: Problem Identification and Resolution577381, Operator Failed to Perform Procedure Step581258, Page 12 of==
: [[SO.]] [[005-3, Revision 1, Routine Inspection of the 3 'A' Recirculation Seal Purge SupplementalCooling SystemSection]]
: ST-O-098-01N-2 Discovered Misplaced
: [[1EP]] [[2: Alert and Notification System (]]
: 568038, SBLC System Inoperable Resulting from Dedicated EO Leaving Area
: [[ANS]] [[) EvaluationPeach Bottom Nuclear Power Plant Upgraded Public Alert and Notification Report, April]]
: 565945, 4 kV Undervoltage Relay Failure and No IR's Written
: [[2005FEMA]] [[]]
: 569879, 4 kV Undervoltage Relay Failure and No IR's Written
: [[ANS]] [[Design Report, December]]
: 576826, NOS Rated PB OPS Yellow For 4Q06
: [[2005EP]] [[-]]
: 581376, Test Aborted: "ECT Portable Pump Operability" RT-O-48B-275-2
: [[MA]] [[-121-1002 "Exelon East Alert and Notification System (ANS) Program," Revision 4]]
: 584506, Through Wall Leak Found on ESW Piping585680, Unit 3 'D' RHR Exceeded the Original Dose Estimate587171,
: [[EP]] [[-]]
: CHK-0-33-515A Not Seated Causes
: [[MA]] [[-121-1004 "Exelon East ANS Corrective Maintenance," Revision 4]]
: ST-0-033-300-2 To Be Aborted
: [[EP]] [[-]]
: 588335, Timeliness/Response to ESW Piping Issue
: [[MA]] [[-121-1005 "Exelon East ANS Preventive Maintenance Program," Revision 3]]
: IR 584506
: [[EP]] [[-]]
: 588800, Weld Verification Deficiency
: [[MA]] [[-121-1006 "Exelon East]]
: 590373, Trng: FME Training Unexcused Absence
: [[ANS]] [[Siren Monitoring, Troubleshooting, and Testing," Revision 5Corrective Maintenance Field Work Instructions for]]
: 590573, E/S 3-17-477 Power Supply Failed Following Swap of 3 'B' RPS
: [[ANS]] [[Control Points, Repeaters and Sirens, Approved December 2004Preventative Maintenance Field Work Instructions for]]
: 593883, Unit 2 'C' RHR Sump Overflowed During Heat Exchange Maintenance
: [[ANS]] [[Control Points, Repeaters and Sirens]]
: 593890, Unit 2 'A' RHR Room Spill During Pumping of the Unit 2 'C' Room Sump
IRs:0043349400565056
: 593891, Unit 2 'C' RHR Sump Overflowed During Heat Exchanger Maintenance
00352078
: 596641, Unusual Event Notification to York County Was > 15 Minutes
005970650048176300451040
: 2264, Mid-Cycle Performance Gap - Self Assessment
00520830
: 606458, Training: PIMS Code Improperly Granted
005213210053315700541478
: 607064, Temperature Recorder
00596641
: TR-0558 not Functional (Discharge Canal)
A-7AttachmentSection
: 615413, Non-Safety-Related Piece Part Installed in Diesel Generator
: [[1EP]] [[4: Emergency Action Level (]]
: 21191, Inadvertent ERO Activation at PBAPS
: [[EAL]] [[) and Emergency Plan ChangesEP-AA-120-1001 "10]]
: 23697, Scaffold Taken to Complete in PIMS But Was Not Removed
: [[CFR]] [[50.54(q) Change Evaluation," Revision 406-12  "]]
: 29910, Late State/Local Notification Made During an EP Drill
: [[ERO]] [[Training and Qualification"]]
: 29970, EAL Classification During Drill Not Timely
: [[TQ]] [[-]]
: 26534, Equipment Not Protected As Required
AA-113, Revision 7
: 596616, Fault at 3 'B' Iso-Phase Cooler Fan Breaker in '4T4' Load Center
06-16  "Radiological Emergency Plan"
: 633532, DDFP/ Engine Trip
: [[EP]] [[-]]
: 604364, Human Error Results in E-3 EDG Overload and E-33 Breaker Trip
AA-1000, Revision 17
 
06-33  "EP Plan Administration"
==Section 4OA3: Event FollowupSpecial Event Procedure (SE)-4, Flood, Revision 21==
: [[EP]] [[-]]
: IR 563253, External Flood Vulnerability - Circulating Water Pump Structure
AA-120, Revision 7
: IR 554800, External Flood Vulnerability Found for EDG Building
06-96  "Emergency Preparedness Advisory Committee"
: IR 520322, E-3 EDG Fire at Roof Exhaust Penetration  
: [[EP]] [[-]]
: A-10AttachmentST-O-37D-370-2, Revision 25, DDFP Operability TestST-O-37D-340-2, Revision 10, DDFP Flow Rate Test
AA-120-1004, Revision 0
: ST-O-37D-340-2, Revision 12, DDFP Flow Rate Test
06-97  "Quarterly Satellite Phone Test"
: ST-M-37D-380-2, Revision 3, DDFP Inspection
: [[EP]] [[-]]
: NOM-C-7.1, Revision 2, Procedure Use
MA-124-1004, Revision 0
: 280-E-8, Revision 16, Single line Meter and relay Diagram, Standby Diesel Generators and4160 Volt Emergency Power System, Unit 26280-E-1615, Revision 64, Single Line Meter and relay Diagram, E-124 and E-224 Emergency Load Centers, E-124-R-C and E-224-R-C Reactor Motor Control Centers, and  
06-99  "EP Fundamentals"
: E-124-T-B and E-224-T-B Turbine Motor Control Centers, 440 Volt, Unit 2Peach Bottom Atomic Power Station Fire Protection Plan, Revision 15
: [[EP]] [[-]]
: A-11AttachmentIssue ReportsIR 00633037IR 00633453
AA-1101, Revision 3
: IR 00633532
06-101"Exelon East
: IR 00634313IR 00634585IR 00634709
: [[ANS]] [[Program"]]
: AR 00635028AR 00635257AR 00635267
EP-MA-121-1002, Revision 4
: AR 00635408
06-102"Exelon East
==LIST OF ACRONYMS==
: [[ANS]] [[Corrective Maintenance Program"]]
ADAMSAgency-wide Documents Access and Management SystemADSautomatic depressurization system
EP-MA-121-1004, Revision 4
ANSAlert and Notification System
06-103"Exelon East
: [[ANS]] [[Preventative Maintenance Program"]]
EP-MA-121-1005, Revision 3
06-108"ERO Fundamentals"
: [[EP]] [[-]]
AA-1102, Revision 2
06-110"Mid-Atlantic
: [[ERO]] [[Notification or Augmentation"]]
EP-AA-112-100-F-07
07-11"Exelon East
: [[ANS]] [[Siren Monitoring, Troubleshooting, and Testing"]]
EP-MA-121-1006, Revision 407-12"ANS Siren Monthly Test" RT-E-101-901-2, Revision 8
07-18"Radiological Emergency Plan Annex for
: [[PBAPS]] [["]]
EP-AA-1007, Revision 14
07-39"Exelon East
: [[ANS]] [[Siren Monitoring, Troubleshooting, and Testing"]]
: [[EP]] [[-MA-121-1006, Revision 5Section]]
: [[1EP]] [[5: Correction of Emergency Preparedness Weaknesses]]
: [[EP]] [[-AA-125 "Emergency Preparedness Self Evaluation Process," Revision4LS-AA-126 "Self-Assessment Program," Revision 5]]
: [[LS]] [[-]]
AA-126-1001 "Focused Area Self-Assessments," Revision 4
Unusual Event Evaluation Reports dated 10/4/06, 11/21/06, 4/16/07
: [[AS]] [[]]
: [[SA]] [[s:  547869, 565747-04]]
: [[NOSA]] [[:-]]
: [[PEA]] [[-06-03 dated 4/13/06]]
: [[NOSA]] [[-]]
PEA-07-04 dated 5/9/07
A-8AttachmentIRs:00433494 00565056
00352078
004817630045104000520830
00533157
005414780059664100597065
00521321Section
: [[1EP]] [[6: Drill EvaluationPeach Bottom Atomic Power Station, May 15, 2007, Off-Year Exercise, Drill ScenarioPeach Bottom Atomic Power Station May 15th, 2007 Off-Year Exercise Report datedJune 14, 2007]]
: [[IR]] [[630584, Enhancement Opportunity from May 2007 EP Drill]]
: [[IR]] [[629910, Late State\Local Notification Made During an]]
: [[EP]] [[Drill]]
: [[IR]] [[629970,]]
EAL Classification During Drill Not Timely
Quick Human Performance Investigation Report,
: [[PB]] [[]]
: [[EAL]] [[Classification During Drill Not Timely, 05/15/07Quick Human Performance Investigation, Repetitive Issue With Not Completing State/Local Notifications on Time, 5/15/07 Section]]
: [[2PS]] [[2 : Radioactive Material Processing and Transportation10]]
CFR Part 61 Sampling and Analysis Results (Waste Streams)Radioactive Material Shipping Documentation
Radioactive Shipping Container Certifications
Audit Template: Chemistry, Radwaste, Effluent and Environmental Monitoring Handling,
Storage and Shipping
Topical Report, Mobile In-container De-watering and Solidification System
DOT-Type A, Test and Evaluation for Type A Packaging
Waste Disposal Facility State Licenses
Training Program - DOT/79-19 Training for Support of Radioactive and Asbestos Shipments
Training Program - Site Specific Portion of Radioactive Material Shipping Training Program Training Program - Shipper Refresher
Type B Cask Handling and Loading Procedures
: [[RT]] [[-W-020-980-2, Updating Radwaste Classification Computer Programs]]
: [[RP]] [[-]]
: [[AA]] [[-605, 10 CFR 61 Compliance Program]]
: [[RP]] [[-]]
: [[AA]] [[-605, 10 CFR 61 Program]]
: [[RP]] [[-]]
: [[PB]] [[-605-1001, Peach Bottom]]
: [[10 CFR]] [[61 SamplingSection 4]]
: [[OA]] [[1: Performance Indicator VerificationLS-AA-2001, Revision 6, Collecting and Reporting of]]
: [[NRC]] [[Performance Indicators Data]]
: [[LS]] [[-AA-2090, Revision 4, Monthly Data Elements for]]
: [[NRC]] [[]]
: [[RCS]] [[Specific Activity]]
: [[LS]] [[-]]
: [[AA]] [[-2100, Revision 5, Monthly Data Elements for]]
: [[NRC]] [[]]
RCS Leakage
ST-O-020-560-2, Reactor Coolant Leakage Test (sample of completed test records)
ST-O-020-560-3, Reactor Coolant Leakage Test (sample of completed test records)
ST-C-095-864-2, Off Gas Monitor Response and Release Rate Verification by a Grab Sample
A-9AttachmentST-C-095-864-3, Off Gas Monitor Response and Release Rate Verification by a Grab SampleST-C-095-820-2, Determination of Dose Equivalent µCi/g I-131 in Primary Coolant
ST-C-095-820-3, Determination of Dose Equivalent µCi/g I-131 in Primary Coolant
CH-407, Sampling of Reactor Water
: [[CH]] [[-C-601, Determination of Dose Equivalent I-131]]
: [[ERO]] [[Drill Participation]]
PI data, April 2006 - March 2007
Public Notification System
: [[PI]] [[data, April 2006 - March 2007]]
: [[DEP]] [[]]
: [[PI]] [[data, April 2006 - March 2007Section]]
: [[4OA]] [[2: Problem Identification and Resolution577381, Operator Failed to Perform Procedure Step581258, Page 12 of]]
ST-O-098-01N-2 Discovered Misplaced
568038,
: [[SBLC]] [[System Inoperable Resulting from Dedicated]]
EO Leaving Area
565945, 4 kV Undervoltage Relay Failure and No IR's Written
569879, 4 kV Undervoltage Relay Failure and No IR's Written
576826,
: [[NOS]] [[Rated]]
PB OPS Yellow For 4Q06
581376, Test Aborted: "ECT Portable Pump Operability" RT-O-48B-275-2
584506, Through Wall Leak Found on
: [[ESW]] [[Piping585680, Unit 3 'D']]
: [[RHR]] [[Exceeded the Original Dose Estimate587171,]]
: [[CHK]] [[-0-33-515A Not Seated Causes]]
ST-0-033-300-2 To Be Aborted
588335, Timeliness/Response to
: [[ESW]] [[Piping Issue]]
IR 584506
588800, Weld Verification Deficiency
590373, Trng: FME Training Unexcused Absence
590573, E/S 3-17-477 Power Supply Failed Following Swap of 3 'B' RPS
593883, Unit 2 'C' RHR Sump Overflowed During Heat Exchange Maintenance
593890, Unit 2 'A' RHR Room Spill During Pumping of the Unit 2 'C' Room Sump
593891, Unit 2 'C' RHR Sump Overflowed During Heat Exchanger Maintenance
596641, Unusual Event Notification to York County Was > 15 Minutes
2264, Mid-Cycle Performance Gap - Self Assessment
606458, Training:
: [[PI]] [[]]
MS Code Improperly Granted
607064, Temperature Recorder TR-0558 not Functional (Discharge Canal)
615413, Non-Safety-Related Piece Part Installed in Diesel Generator
21191, Inadvertent
: [[ERO]] [[Activation at]]
: [[PBAPS]] [[23697, Scaffold Taken to Complete in]]
: [[PI]] [[]]
MS But Was Not Removed
29910, Late State/Local Notification Made During an EP Drill
29970, EAL Classification During Drill Not Timely
26534, Equipment Not Protected As Required
596616, Fault at 3 'B' Iso-Phase Cooler Fan Breaker in '4T4' Load Center
633532,
: [[DD]] [[]]
FP/ Engine Trip
604364, Human Error Results in E-3
: [[EDG]] [[Overload and E-33 Breaker TripSection 4]]
: [[OA]] [[3: Event FollowupSpecial Event Procedure (SE)-4, Flood, Revision 21 IR 563253, External Flood Vulnerability - Circulating Water Pump Structure]]
: [[IR]] [[554800, External Flood Vulnerability Found for]]
: [[EDG]] [[Building]]
: [[IR]] [[520322, E-3]]
EDG Fire at Roof Exhaust Penetration
A-10AttachmentST-O-37D-370-2, Revision 25,
: [[DDFP]] [[Operability Test]]
: [[ST]] [[-O-37D-340-2, Revision 10,]]
: [[DD]] [[]]
: [[FP]] [[Flow Rate Test]]
: [[ST]] [[-O-37D-340-2, Revision 12,]]
: [[DDFP]] [[Flow Rate Test]]
: [[ST]] [[-M-37D-380-2, Revision 3,]]
DDFP Inspection
NOM-C-7.1, Revision 2, Procedure Use
280-E-8, Revision 16, Single line Meter and relay Diagram, Standby Diesel Generators and4160 Volt Emergency Power System, Unit 26280-E-1615, Revision 64, Single Line Meter and relay Diagram, E-124 and E-224 Emergency Load Centers, E-124-R-C and E-224-R-C Reactor Motor Control Centers, and
E-124-T-B and E-224-T-B Turbine Motor Control Centers, 440 Volt, Unit 2Peach Bottom Atomic Power Station Fire Protection Plan, Revision 15
A-11AttachmentIssue ReportsIR 00633037IR 00633453
: [[IR]] [[00633532]]
: [[IR]] [[00634313]]
: [[IR]] [[00634585IR 00634709]]
: [[AR]] [[00635028]]
: [[AR]] [[00635257AR 00635267]]
: [[AR]] [[00635408]]
: [[LIST]] [[]]
: [[OF]] [[]]
: [[ACRONY]] [[MSADAMSAgency-wide Documents Access and Management SystemADSautomatic depressurization system]]
: [[AN]] [[]]
SAlert and Notification System
ARaction request
ARaction request
BTPsbranch technical positions
BTPsbranch technical positions
: [[CAP]] [[corrective action program]]
CAPcorrective action program
: [[CF]] [[]]
CFRCode of Federal Regulations
RCode of Federal Regulations
CRcondition report
CRcondition report
CRDcontrol rod drive
CRDcontrol rod drive
CSTcondensate storage tank
CSTcondensate storage tank
: [[DBD]] [[sDesign Basis Documents]]
DBDsDesign Basis Documents
: [[DD]] [[]]
DDFPdiesel-driven fire pump
: [[FP]] [[diesel-driven fire pump]]
DEPDrill and Exercise Performance
: [[DE]] [[]]
DOTDepartment of Transportation
: [[PD]] [[rill and Exercise Performance]]
DRPDivision of Reactor Projects
: [[DO]] [[]]
: [[TD]] [[epartment of Transportation]]
: [[DR]] [[]]
PDivision of Reactor Projects
EALemergency action level
EALemergency action level
EDGemergency diesel generator
EDGemergency diesel generator
EPemergency preparedness
EPemergency preparedness
EROemergency response organization
EROemergency response organization
: [[ESW]] [[emergency service water]]
ESWemergency service water
: [[HP]] [[]]
HPCIhigh pressure coolant injection
: [[CI]] [[high pressure coolant injection]]
HPSWhigh pressure service water
: [[HP]] [[]]
HCUhydraulic control unit
SWhigh pressure service water
IMCInspection Manual Chapter
: [[HCU]] [[hydraulic control unit]]
: [[IM]] [[]]
CInspection Manual Chapter
IPInspection Procedure
IPInspection Procedure
IRissue report
IRissue report
Line 1,490: Line 762:
MRMaintenance Rule
MRMaintenance Rule
MSmitigating system
MSmitigating system
: [[NCV]] [[noncited violation]]
NCVnoncited violation
: [[NE]] [[]]
NEINuclear Energy Institute
: [[IN]] [[uclear Energy Institute]]
NRCNuclear Regulatory Commission
: [[NR]] [[]]
CNuclear Regulatory Commission
OCsoperator challenges
OCsoperator challenges
OWAsoperator work-arounds
OWAsoperator work-arounds
: [[PAR]] [[protective action recommendation]]
PARprotective action recommendation
: [[PAR]] [[]]
PARSPublicly Available Records
: [[SP]] [[ublicly Available Records]]
PBAPSPeach Bottom Atomic Power Station
: [[PBAP]] [[]]
PCIVprimary containment isolation valve
: [[SP]] [[each Bottom Atomic Power Station]]
PCPProcess Control Program
: [[PC]] [[]]
: [[IV]] [[primary containment isolation valve]]
: [[PC]] [[]]
PProcess Control Program
2AttachmentPIperformance indicatorPMTpost-maintenance testing
2AttachmentPIperformance indicatorPMTpost-maintenance testing
PROplant reactor operator
PROplant reactor operator
: [[RB]] [[reactor building]]
RBreactor building
: [[RC]] [[]]
RCICreactor core isolation cooling
ICreactor core isolation cooling
RCRroot cause report
RCRroot cause report
RCSreactor coolant system
RCSreactor coolant system
Line 1,518: Line 783:
RRPreactor recirculation pump
RRPreactor recirculation pump
RTPrated thermal power
RTPrated thermal power
: [[SDP]] [[significance determination process]]
SDPsignificance determination process
: [[SJ]] [[]]
SJAEsteam jet-air ejector
: [[AE]] [[steam jet-air ejector]]
SPACstandards, policies, and administrative controls
: [[SP]] [[]]
ACstandards, policies, and administrative controls
SOsystem operating
SOsystem operating
SSCsstructures, systems, and components
SSCsstructures, systems, and components
SRVsafety relief valve
SRVsafety relief valve
: [[ST]] [[ssurveillance tests]]
STssurveillance tests
: [[TR]] [[]]
TRMTechnical Requirements Manual
MTechnical Requirements Manual
TRTtroubleshooting, rework and testing
TRTtroubleshooting, rework and testing
TSTechnical Specification
TSTechnical Specification
TSCtechnical support center
TSCtechnical support center
UEunusual event
UEunusual event
: [[URI]] [[unresolved item]]
URIunresolved item
: [[UFSA]] [[]]
UFSARUpdated Final Safety Analysis Report
RUpdated Final Safety Analysis Report
USQunreviewed safety question
USQunreviewed safety question
: [[WO]] [[work order]]
: [[WO]] [[work order]]
}}
}}

Revision as of 01:56, 23 October 2018

IR 05000277-07-003, 05000278-07-003, 04/01/2007 - 06/30/2007, Peach Bottom Atomic Power Station (Pbaps), Units 2 & 3; Event Followup
ML072120599
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 07/30/2007
From: Krohn P G
Reactor Projects Region 1 Branch 4
To: Crane C M
Exelon Generation Co, Exelon Nuclear
KROHN P G, RI/DRP/PB4/610-337-5120
References
IR-07-003
Download: ML072120599 (22)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION REGION I475 ALLENDALE ROADKING OF PRUSSIA, PENNSYLVANIA 19406-1415 July 30, 2007 Mr. Christopher President and CNO Exelon NuclearExelon Generation Company, LLC200 Exelon Way Kennett Square, PA 19348

SUBJECT: PEACH BOTTOM ATOMIC POWER STATION - NRC INTEGRATED INSPECTION REPORT 05000277/2007003 AND 05000278/2007003

Dear Mr. Crane:

On June 30, 2007, the United States Nuclear Regulatory Commission (NRC) completed aninspection at your Peach Bottom Atomic Power Station (PBAPS), Units 2 and 3. The enclosedintegrated inspection report documents the inspection results, which were discussed on July 20, 2007, with Mr. J. Grimes and other members of your staff.The inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. The report documents three self-revealing findings of very low safety significance (Green). Two ofthese findings were determined to involve violations of NRC requirements. Additionally, threelicensee-identified violations which were determined to be of very low safety significance are listedin this report. However, because of the very low safety significance and because they are entered into your corrective action program (CAP), the NRC is treating these findings as non-citedviolations (NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contestany NCV in this report, you should provide a response within 30 days of the date of this inspectionreport, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: DocumentControl Desk, Washington, D.C. 20555-0001; with copies to the Regional Administrator, Region I;the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington,D.C. 20555-0001; and the NRC Resident Inspector at Peach Bottom.

C. M. Crane2In accordance with 10 Code of Federal Regulations (CFR) 2.390 of the NRC's "Rules of Practice,"a copy of this letter, its enclosures, and your response (if any) will be available electronically forpublic inspection in the NRC Public Document Room or from the Publicly Available Records(PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from theNRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic ReadingRoom).

Sincerely,/RA/Paul G. Krohn, Chief Reactor Projects Branch 4Division of Reactor ProjectsDocket Nos.:50-277, 50-278License Nos.:DPR-44, DPR-56

Enclosures:

Inspection Report 05000277/2007003 and 05000278/2007003

w/Attachment:

Supplemental Informationcc w/encl:Chief Operating Officer, Exelon Generation Company, LLC Site Vice President, Peach Bottom Atomic Power Station Plant Manager, Peach Bottom Atomic Power Station Regulatory Assurance Manager - Peach Bottom Manager, Financial Control & Co-Owner Affairs Vice President, Licensing and Regulatory Affairs Senior Vice President, Mid-Atlantic Senior Vice President - Operations Support Director, Licensing and Regulatory Affairs J. Bradley Fewell, Assistant General Counsel, Exelon Nuclear Manager Licensing, PBAPS Director, Training Correspondence Control Desk Director, Bureau of Radiation Protection, Department of Environmental Protection R. McLean, Power Plant and Environmental Review Division (MD)

G. Aburn, Maryland Department of Environment T. Snyder, Director, Air and Radiation Management Administration, MD Department of the Environment Public Service Commission of Maryland, Engineering Division Board of Supervisors, Peach Bottom Township B. Ruth, Council Administrator of Harford County Council Mr. & Mrs. Dennis Hiebert, Peach Bottom Alliance TMI - Alert (TMIA)

J. Johnsrud, National Energy Committee, Sierra Club Mr. & Mrs. Kip Adams E. Epstein, TMI Alert R. Fletcher, Department of Environment, Radiological Health Program C. M. Crane2In accordance with 10 Code of Federal Regulations (CFR) 2.390 of the NRC's "Rules of Practice," a copy ofthis letter, its enclosures, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/r eading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA/Paul G. Krohn, Chief Reactor Projects Branch 4 Division of Reactor ProjectsDocket Nos.:50-277, 50-278License Nos.:DPR-44, DPR-56

Enclosures:

Inspection Report 05000277/2007003 and 05000278/2007003

w/Attachment:

Supplemental InformationDistribution w/encl:S. Collins, RAR. Fuhrmeister, DRP M. Dapas, DRAT. Setzer, DRP J. Lamb, RI OEDO F. Bower, DRP - Senior Resident Inspector H. Chernoff, NRRM. Brown, DRP - Resident Inspector J. Hughey NRR, PMS. Schmitt - Resident OA P. Bamford, PM, BackupRegion I Docket Room (with concurrences)

J. Lubinski, NRRROPreports@nrc.govP. Krohn, DRP SUNSI Review Complete: __PGK_______ (Reviewer's Initials)DOCUMENT NAME: C:\FileNet\ML072120599.wpdAfter declaring this document "An Official Agency Record" it will be released to the Public.To receive a copy of this document, indicate in the box:

" C" = Copy without attachment/enclosure " E" =Copy with attachment/enclosure " N" = No copyML072120599OFFICERI/DRP Rl/DRP NAMEFbower/PGK forPKrohn/PGKDATE07/24/0707/24/07OFFICIAL RECORD COPY U. S. NUCLEAR REGULATORY COMMISSIONREGION IDocket Nos.:50-277, 50-278 License Nos.:DPR-44, DPR-56 Report No.:05000277/2007003 and 05000278/2007003 Licensee:Exelon Generation Company, LLC Facility:Peach Bottom Atomic Power Station (PBAPS), Units 2 and 3 Location:Delta, Pennsylvania Dates:April 1, 2007 through June 30, 2007 Inspectors:F. Bower, Senior Resident InspectorM. Brown, Resident Inspector R. Fuhrmeister, Senior Project Engineer R. Nimitz, Senior Health Physicist N. Perry, Sr. Emergency Response Coordinator R. Cureton, Emergency Preparedness InspectorApproved by:Paul G. Krohn, ChiefReactor Projects Branch 4 Division of Reactor Projects ii

SUMMARY OF FINDINGS

IR 05000277/2007-003, 05000278/2007-003; 04/01/2007 - 06/30/2007; Peach Bottom AtomicPower Station (PBAPS), Units 2 and 3; Event Followup. The report covered a 3-month period of inspection by resident inspectors, a senior projectengineer, and announced inspections by a senior health physicist, a senior emergency response coordinator, and an emergency preparedness inspector. Three Green findings, two of which were NCVs, were identified. The significance of most findings is indicated by their color (Green,

White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006. A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green.

A self-revealing finding was identified for inadequate implementation ofwork order (WO) instructions to verify the correct breaker frame size during the overhaul of a compatible spare breaker for installation into the '4T4' 480 volt load center. This condition resulted in a poor electrical connection between the primary disconnect fingers and the switchgear bus stabs for one breaker in the '4T4' load center that ultimately resulted in a fire that led to a plant transient and declaration of an Unusual Event (UE).This finding is greater than minor because it affected the human performanceattribute of the Initiating Event Cornerstone, in that, an incorrect frame size breaker was installed into a cubicle for which it was not sized. This mismatch caused an electrical fault that led to a fire and a plant transient that upset plant stability. The finding was of very low safety significance (Green) because it did not increase both the likelihood of a reactor scram and that mitigation equipment or functions would not be available. The inspectors determined that this finding had a cross-cutting aspect in the area of human performance (work practices component) because maintenance technicians did not follow WO instructions to specifically verify the frame size of a breaker during its overhaul (IMC 0305 aspect H.4(b)). (Section 4OA3.1)*Green. A self-revealing NCV of Technical Specification (TS) 5.4.1, was identifiedwhen operators inadequately implemented a surveillance test by missing a procedure step. The missed step placed the E-3 emergency diesel generator (EDG) in the isochronous mode of operation while it was synchronized to off-site power and resulted in an unexpected over-loading of the E-3 EDG. This finding is more than minor because it was associated with the humanperformance attribute of the Mitigating Systems Cornerstone, and impacted the cornerstone objective of ensuring the availability of the E-3 EDG to respond to initiating events. This finding is of very low safety significance (Green) because all other EDGs remained operable and the actual loss of safety function of the E-3 EDG was less than the TS allowed outage time of seven days. The inspectors ivdetermined that this finding had a cross-cutting aspect in the area of humanperformance (work practices component) because PBAPS personnel did not follow procedures when the E-3 EDG was placed in the isochronous load control mode with the E-3 EDG in parallel with the off-site power source (IMC 0305 aspect H.4(b)). (Section 4OA3.2)*Green. A self-revealing NCV of TS 5.4.1, was identified when operatorsmanipulated a diesel-driven fire pump (DDFP) cooling water valve outside of procedure guidance. The improper manipulation led to misalignment of the DDFP cooling water that subsequently damaged the engine during operations without cooling water. The failure to use a procedure for cleaning and restoring the DDFP cooling waterstrainer was a more than minor finding because it was associated with the degradation of a fire protection feature, in that, the DDFP was rendered inoperable by damage to the engine. Using the Fire Protection SDP, the finding was determined to be of very low safety significance due to the motor-driven fire pump remaining operable during the five days the DDFP was inoperable, and the small number of fire scenarios which would impact the power supply to the motor-driven fire pump. This finding had a cross-cutting aspect in the area of human performance (resources component) because procedure ST-O-37D-340-2 did not provide complete and accurate instructions for cleaning the DDFP cooling water strainer (IMC 0305 aspect H.2©). (Section 4OA3.3)

B.Licensee-Identified Violations

Three violations of very low safety significance (Green), that were identified by thelicensee, have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's CAP. The violations and corrective actions are listed in Section 4OA7 of this report.

Enclosure

REPORT DETAILS

Summary of Plant StatusUnit 2 began the inspection period at 100 percent full rated thermal power (RTP) until April 27, 2007, when power was reduced to 58 percent for planned waterbox cleaning, control rod testing, 2 'A' reactor feed pump (RFP) maintenance, and other planned maintenance and testing. On April 28, 2007, the unit returned to full power where it remained until the end of the inspection period, except for brief periods to support planned testing and rod pattern adjustments. Unit 3 began the inspection period at 100 percent full RTP until April 16, 2007, when anunplanned power reduction to 84 percent was performed in response to rapidly increasing 3 'A' reactor recirculation pump shaft seal temperatures. The unit returned to full power on April 18, 2007. On May 4, 2007, power was reduced to 59 percent for planned waterbox cleaning, control rod testing, and 3 'C' RFP maintenance. The unit returned to full power on May 5, 2007. On May 11, 2007, power was reduced to 65 percent for a planned control rod pattern adjustment and RFP testing, and the unit returned to full power on May 12, 2007. On June 15, 2007, power was reduced to 82 percent for a rod pattern adjustment and planned maintenance on a feedwater heater drain line. The unit was returned to full power on June 16, 2007, where it remained until the end of the inspection period, except for brief periods to support planned testing and rod pattern adjustments.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity1R01Adverse Weather Protection (71111.01 - 1 System Sample; 1 Site Sample).1Summer Seasonal Readiness

a. Inspection Scope

The inspectors performed one seasonal readiness sample that included a review of threeventilation systems. Specifically, the inspectors reviewed the procedures listed in 1 to the report, and verified summer ventilation system alignment for the diesel generator building, circulating water pump structure, and circulating water pump screen house.

b. Findings

No findings of significance were identified.

2Enclosure.2Adverse Weather Event Review

a. Inspection Scope

On June 13, 2007, a tornado warning was issued for an adjacent county. The inspectorsreviewed PBAPS's actions taken to respond to potential adverse environmental conditions from severe thunderstorms that entered the area. High winds, lightning, rain, and reports of hail were experienced at the site. The inspectors observed that PBAPS's personnel consulted procedure OP-PB-108-111-1001, "Preparation for Severe Weather," increased the online risk assessment to "Yellow," and subsequently implemented procedure AO 53.2-0, "Equipment Checks After a Thunderstorm."

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment (71111.04Q - 3 Partial Walkdown Samples).1Partial Walkdown

a. Inspection Scope

The inspectors performed a partial walkdown of three systems to verify the operability ofredundant or diverse trains and components when safety-related equipment was inoperable. The inspectors performed walkdowns to identify any discrepancies that could impact the function of the system and potentially increase risk. The inspectors reviewed applicable operating procedures, walked down system components, and verified that selected breakers, valves, and support equipment were in the correct position to support system operation. The inspectors also verified that PBAPS had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the CAP. The three systems reviewed were: *E-3 Diesel Generator and 3 Startup Transformer with the 2 Startup TransformerOut-of-Service;*Unit 2 Reactor Core Isolation Cooling (RCIC) with Unit 2 High Pressure CoolantInjection (HPCI) Out-of-Service; and*'B' Emergency Service Water (ESW) with 'A' ESW Out-of-Service.

b. Findings

No findings of significance were identified..2Complete System Walkdown (71111.04S - 1 Sample)

a. Inspection Scope

During the week of June 25, 2007, the inspectors performed one complete Unit 2 highpressure service water (HPSW) system walkdown of the accessible portions of the 3Enclosuresystem. The full walkdown was performed to identify any discrepancies which couldimpact the Unit 2 HPSW system function. The inspectors reviewed system operating procedures, piping and instrumentation drawings, walked down control system components, and verified that circuit breakers and valves were in the appropriate positions.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05Q - 10 Samples)Fire Protection - Tours

a. Inspection Scope

The inspectors reviewed PBAPS's Fire Protection Plan, Technical Requirements Manual(TRM), and the respective pre-fire action plan procedures to determine the required fire protection design features, fire area boundaries, and combustible loading requirements for the areas examined during this inspection. The fire risk analysis was reviewed to gain risk insights regarding the areas selected for inspection. The inspectors performed walkdowns of ten areas to assess the material condition of active and passive fire protection systems and features. The inspection was also performed to verify the adequacy of the control of transient combustible material and ignition sources, the condition of manual firefighting equipment, fire barriers, and the status of any related compensatory measures. The following ten fire areas were reviewed for impaired fire protection features:*Unit 3 Reactor Building (RB), RCIC Room, 88' Elevation (Fire Zone 63);*Standby Gas Treatment Room, Radwaste Building, 91'6" Elevation (Fire Zone 70);

  • Unit 3 RB, North Control Rod Drive (CRD) Equipment and West Corridor (Fire Zone 13H);*Unit 3 Refuel Floor (Fire Zone 55);
  • Unit 3 'A' and 'C' Core Spray Rooms (Fire Zones 13D & 13E);
  • Unit 2 Emergency Battery/Switchgear Rooms (Fire Zone 127);
  • Unit 2 RCIC (Fire Zone 60);
  • 2 Startup Switchgear Building (Fire Zone 164); and
  • Diesel Generator Building, 127' Elevation (Fire Zone 132).

b. Findings

No findings of significance were identified.

4Enclosure1R11Licensed Operator Requalification Program (71111.11Q - 1 Sample) Resident Inspector Quarterly Review

a. Inspection Scope

On June 12, 2006, the inspectors observed operators in PBAPS's simulator duringlicensed operator requalification training to verify that operator performance was adequate and that evaluators were identifying and documenting crew performance issues. The inspectors verified that performance issues were discussed in the crew's post-scenario critiques. The inspectors also observed operator implementation of procedures. The inspectors discussed the training, simulator scenarios, and critiques with the operators, shift supervision, and the training instructors. The evaluated scenario observed for this one sample involved the events listed below: *Small Break Loss of Coolant Accident; and*An Anticipated Transient Without Scram.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12Q - 2 Samples)

a. Inspection Scope

The inspectors reviewed two samples of PBAPS's evaluation of degraded conditionsinvolving safety-related structures, systems, and components (SSCs) for maintenance effectiveness during this inspection period. The inspectors reviewed PBAPS's implementation of the Maintenance Rule (MR), and verified that the conditions associated with the referenced condition reports (CRs) were evaluated against applicable MR functional failure criteria as found in the licensee's scoping documents and procedures.

The inspectors also discussed these issues with system engineers and MR coordinators to verify that they were tracked against performance criteria and that the systems were classified in accordance with MR implementation guidance. Documents reviewed during the inspection are listed in the Attachment. The following conditions were reviewed:*Issue Report (IR) 587171, ESW Check Valve (CHK-0-33-515A) - Not SeatedCauses ESW ST-O-033-300-2 to be Aborted; and*IR 622560, Maintenance Preventable Functional Failure for Loss of '4T4' 480 VoltLoad Center.

b. Findings

No findings of significance were identified.

5Enclosure1R13Maintenance Risk Assessments and Emergent Work Control (71111.13 - 8 Samples)

a. Inspection Scope

The inspectors evaluated PBAPS's implementation of their maintenance risk program toverify that PBAPS managed risk in accordance with 10 CFR Part 50.65(a)(4). Procedure WC-AA-101, "On-line Work Control Process," was also reviewed. This inspection included reviews of PBAPS's use of the Paragon online risk monitoring software. The inspectors reviewed equipment tracking documentation, daily work schedules, and performed plant tours. The following activities selected were based on plant maintenance schedules and systems that contributed to risk. The inspectors completed eight evaluations of maintenance activities on the following:*Troubleshooting, Rework and Testing (TRT) Control Form No. 07-18, Monitor3 'A' Recirculation Pump Seal Parameters During Recirculation Pump Speed Changes;*TRT No.07-020, Re-align CRD Pump Suction to the Condensate Storage Tank(CST) from the Condensate System;*WO C0220911, Calibrate, Repair & Replace E-2 EDG Temperature Switch;

  • WO A1613202, 3 'B' Recirculation Pump 2 nd Stage Seal Pressure;*IR 623723, Bolt and Heli-coil Found Damaged at Disassembly on 00T634;
  • IR 626534, Equipment Not Protected As Required;
  • WO R0736769-01, Core Spray Loop 'A' Full Flow Test Valve Operator,MO-2-14-026A-OP, Perform Motor Operator Preventive Maintenance; and*IR 542109, 2 'C' Service Air Compressor Trip.Additionally, the inspectors verified that an inspector-identified issue, IR 626534,"Equipment Not Protected As Required," was entered into the PBAPS's CAP.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15 - 5 Samples)

a. Inspection Scope

The inspectors reviewed five issues to assess the technical adequacy of the evaluations,the use and control of compensatory measures, and compliance with the licensing and design bases. Associated adverse condition monitoring plans, engineering technical evaluations, and operational and technical decision making documents were also reviewed. The inspectors verified these processes were performed in accordance with the applicable procedures. The inspectors used TS, TRM, the Updated Final Safety Analysis Report (UFSAR), and associated Design Basis Documents (DBDs) as referencesduring these reviews. The issues reviewed included:*Non-Safety Related Piece Installed in E-4 EDG Part (IR 615413);*Rising 3 'A' Reactor Recirculation Pump (RRP) #2 Seal Temperature (IR 617988);

  • Provide Supplemental Cooling to the 3 'A' RRP Seal (IR 618478);

6EnclosureTarget Rock Safety/Relief Valve (SRV) Seal Welds: Potential Code Issue(IR 628251); andSmall Leak on 2 'B' Main Steam Line Differential Pressure Instrument LineSnubber Threaded Cap (IR 627026).

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing (71111.19 - 7 Samples)

a. Inspection Scope

The inspectors observed selected portions of post-maintenance testing (PMT) activitiesand reviewed completed test records. The inspectors observed whether the tests were performed in accordance with the approved procedures and assessed the adequacy of the test methodology based on the scope of maintenance work performed. In addition, the inspectors assessed the test acceptance criteria to evaluate whether the test demonstrated that the tested components satisfied the applicable design and licensing bases and the TS requirements. The inspectors reviewed the recorded test data to verify that the acceptance criteria were satisfied. The inspectors reviewed seven PMTs performed in conjunction with the following maintenance activities:*WO C0220911, Calibrate, Repair & Replace E-2 EDG Temperature Switch;*WO R1049367, Unit 3 Hydraulic Control Unit (HCU) 50-43: HCU Overhaul;

  • WO C0216504, RCIC Suction Pressure Switch (PS-2-13-067-01), Replace Pressure Switch; WO C0221445, Inspect/Repair/Replace Unit 2 'C' Main Steam Line Radiation Monitor (RIS-2-17-251C);*WO C0215740, Replace Unit 2 'B' Reactor Protection System Motor Generator Set Endbell; and*WO R0629147, Perform Motor Control Unit Inspection on the 'C' Glycol Pump.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22 - 5 Samples) [3 Routine Samples; 1 IST Sample; 1Reactor Coolant System (RCS) Leakage Sample]

a. Inspection Scope

The inspectors reviewed and observed portions of selected surveillance tests (STs), andcompared test data with established acceptance criteria to verify the systems demonstrated the capability of performing the intended safety functions. The inspectors also verified that the systems and components maintained operational readiness, met applicable TS requirements, and were capable of performing the design basis functions.

The five STs reviewed and observed included:

7Enclosure*ST-O-023-301-3, HPCI Pump, Valve, Flow and Unit Cooler Functional andIn-Service Test [IST Sample];*ST-O-020-560-2 & 3, Reactor Coolant Leakage Test [RCS Leakage Sample];

  • ST-I-60A-230-3, Linear Power Range Monitor Gain Calibration;
  • SI2T-MIS-8547-C1CQ, Calibration/Functional Check of Channel 'C' Group 1, 4and 5 of Primary Containment Isolation Valve (PCIV) Logic for TSs-80547C; and*ST-R-003-485-3, CRD Scram Insertion Timing of Selected Control Rods.b.FindingsNo findings of significance were identified.

1R23 Temporary Plant Modifications (71111.23 -1 Sample)

a. Inspection Scope

The inspectors reviewed one temporary modification to verify that implementation of themodification did not place the plant in an unsafe condition. The review was also conducted to verify that the design bases, licensing bases, and performance capability ofrisk significant SSCs had not been degraded as a result of the modification. The inspectors verified the modified equipment alignment through control room instrumentation observations; the UFSAR; drawings; procedures; WO reviews; and plant walkdowns of accessible equipment. The following temporary modification was reviewed:*TCCP 07-00172, Install Cooling Unit to Assist 3 'A' RRP Seal Cooling.

b. Findings

No findings of significance were identified.Cornerstone: Emergency Preparedness1EP2Alert and Notification System (ANS) Evaluation (71114.02 - 1 Sample)

a. Inspection Scope

An onsite review was conducted to assess the maintenance and testing of the PBAPS'sANS. During this inspection, the inspectors interviewed emergency preparedness (EP)staff responsible for implementation of the ANS testing and maintenance. IRs pertaining to the ANS were reviewed for causes, trends, and corrective actions. The inspectors further discussed with PBAPS, the ANS siren system and its performance from July 2005 through May 2007. The inspectors reviewed the licensee's procedures and the ANS design report to ensure compliance with those commitments for system maintenance and testing. The inspection was conducted in accordance with NRC Inspection Procedure (IP)71114, Attachment 2. Planning standard, 10 CFR 50.47(b)(5) and the related requirements of 10 CFR 50, Appendix E were used as reference criteria.

b. Findings

No findings of significance were identified.1EP3Emergency Response Organization (ERO) Staffing and Augmentation System (71114.03 - 1 Sample)

a. Inspection Scope

A review of Peach Bottom's ERO augmentation staffing requirements and the process fornotifying the ERO was conducted. This was performed to ensure the readiness of key staff for responding to an event and to ensure timely facility activation. The inspectors reviewed procedures and IRs associated with the ERO notification system and drills, and reviewed records from call-in drills. The inspectors interviewed personnel responsible for testing the ERO augmentation process, and reviewed the training records for a sampling of the ERO to ensure training and qualifications were up-to-date. The inspectors reviewed procedures for ERO administration and training, and verified a sampling of the ERO participated in exercises in 2005 and 2006. The inspectors also reviewed records of offsite agency training and the June 2007 Respirator Qualification Report. The inspection was conducted in accordance with NRC IP 71114, Attachment 3. Planning standard, 10 CFR 50.47(b)(2) and related requirements of 10 CFR 50, Appendix E were used as reference criteria.

b. Findings

No findings of significance were identified. 1EP4Emergency Action Level (EAL) and Emergency Plan Changes (71114.04 - 1 Sample)

a. Inspection Scope

Since the last NRC inspection of this program area, Emergency Plan (Plan), Revision 26,was implemented based on PBAPS's determination, in accordance with 10 CFR 50.54(q), that the changes resulted in no decrease in effectiveness of the Plan, and that the revised Plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR 50. The inspectors conducted a sampling review of the Emergency Plan changes, and changes to the lower-tier Emergency Plan implementing procedures, to evaluate the changes for potential decreases in effectiveness of the Emergency Plan. However, this review was not documented in a safety evaluation report and does not constitute formal NRC approval of the changes. Therefore, these changes remain subject to future NRC inspection in their entirety.

b. Findings

No findings of significance were identified.

9Enclosure1EP5Correction of Emergency Preparedness Weaknesses (71114.05 - 1 Sample)

a. Inspection Scope

The inspectors reviewed a sampling of self-assessment procedures and reports to assessPBAPS's ability to evaluate their performance and programs. The inspectors reviewed a sampling of IRs from July 2006 through May 2007, initiated by Exelon Nuclear at Peach Bottom from drills, self-assessments, and audits. Other drill reports reviewed included:

medical/health physics, fire, integrated, and call-in.

Additionally, the inspectors reviewed the three UE Evaluation Reports generated since the last inspection, and audits for 2006 and 2007 required by 50.54(t). This inspection was conducted in accordance with NRC IP 71114, Attachment 5. Planning standard, 10 CFR 50.47(b)(14) and the related requirements of 10 CFR 50, Appendix E were used as reference criteria.

b. Findings

No findings of significance were identified.1EP6Drill Evaluation (71114.06 - 1 Sample)Off-Year Exercise (Drill)

a. Inspection Scope

The inspectors conducted this inspection to assess: training quality and conduct;emergency plan procedure implementation; facility and equipment readiness; personnel performance in drills and exercises; organizational and management changes; and communications equipment readiness. The primary focus of this inspection was to verify PBAPS's critique of classification, notification, and protective action recommendation (PAR) development.On May 15, 2007, the inspectors observed a full scale drill. The primary focus of thisinspection was to verify PBAPS's critique of classification, notification, and PAR development. Selected portions of the drill were observed in the control room simulator and later in the technical support center (TSC). The drill scenario began with a simulated internal flooding event in the 2 'A' residual heat removal (RHR) pump room that degraded the performance of the associated safety system. The drill scenario continued with a simulated reactor event that started with a reduction of coolant flow to the core and progressed until three fission product barriers (fuel cladding, RCS, and containment) were lost.

The inspectors observed licensed operator and ERO personnel adherence to the Emergency Plan implementing procedures. The ERO personnel responses to simulated degraded plant conditions were inspected to identify weaknesses and deficiencies in classification and notification. The inspectors also observed the transition of responsibility for the ERO from the shift manager in the simulated control room to the TSC. The inspectors observed PBAPS's critique of the drill to evaluate PBAPS's identification of weaknesses and deficiencies. The inspectors compared PBAPS's identified issues against the inspectors' observations to determine whether PBAPS adequately identified problems and entered them into the CAP. This inspection activity represented one 10Enclosuresample. The documents and procedures reviewed during the inspection are listed in theAttachment.

b. Findings

No findings of significance were identified.2.RADIATION SAFETYCornerstone: Public Radiation Safety 2PS2Radioactive Material Processing and Transportation (71122.02 - 5 Samples).1Inspection Planning/In-Office Inspection

a. Inspection Scope

The inspectors reviewed the solid waste system description in the UFSAR and recentradiological effluent release reports for information on the types and amounts of radioactive waste. The inspectors reviewed Exelon's audit program in the area of radioactive wastecharacterization, transportation, and disposal. The inspectors also reviewed the status of the NRC approved quality assurance program in this area. (Section 2PS2.6)

b. Findings

No findings of significance were identified.

.2 Radioactive Waste System Walkdown

a. Inspection Scope

The inspectors walked down accessible portions of the station's radioactive liquid andsolid waste collection, processing, and storage systems and locations to determine if:

systems and facilities were consistent with descriptions provided in the UFSAR; to evaluate their general material conditions; and to identify changes made to systems.

Areas visually inspected included tank and pump rooms, the de-watering facility, in-plant and outside waste storage areas, outside tank areas, and the low level-waste storage facility. Visual inspection records and previous surveys were also reviewed. The inspector also discussed operation of the radwaste systems with cognizant licensee personnel.The inspectors reviewed the status of any non-operational or abandoned radioactivewaste process equipment; the adequacy of administrative and physical controls for those systems; changes made to radioactive waste processing systems and potential radiological impact, including conduct of safety evaluations of the changes, as necessary.

11EnclosureThe inspectors reviewed the current processes for transferring radioactive waste resin andsludge to shipping containers and mixing and sampling of the waste, as appropriate, to evaluate waste mixing, adequacy of sampling, and the methodology for waste concentration averaging. The inspector also reviewed radioactive waste and material storage and handling practices; sources of radioactive waste at the station (waste streams) and processing (as appropriate) and handling of the waste; and the general condition of facilities and equipment. The review was against criteria contained in the station's UFSAR, 10 CFR Part 20,10 CFR 61, the Process Control Program (PCP), and applicable station procedures.

b. Findings

No findings of significance were identified..3Waste Characterization and Classification

a. Inspection Scope

The inspector reviewed the following matters:

  • Radio-chemical sample analysis results for radioactive waste streams;*Development of scaling factors for difficult to detect and measure radionuclides;
  • Methods and practices to detect changes in waste streams;
  • Classification and characterization of waste relative to 10 CFR 61.55 and 10 CFR 61.56;*Implementation of applicable NRC branch technical positions (BTPs) on wasteclassification, concentration averaging, waste stream determination, and sampling frequency;*Current waste streams and their processing relative to descriptions contained inthe UFSAR and the station's approved PCP; *Current processes for transferring radioactive waste resin and sludge dischargesinto shipping/disposal containers to determine adequacy of sampling; *Revisions of the PCP and the UFSAR to reflect changes (as appropriate); and
  • Waste processing topical report (de-watering).The inspector discussed the adequacy of samples collected from the waste transfer andde-watering system.The review was against criteria contained in 10 CFR 20, 10 CFR 61, 10 CFR 71, the UFSAR, the PCP, applicable NRC BTPs, and Exelon procedures.

b. Findings

No findings of significance were identified.

12Enclosure.4Shipment Preparation

a. Inspection Scope

The inspector observed a non-exempt radioactive material shipment (PM-07-057) inpreparation. The inspector reviewed associated transportation documents, reviewed radiological surveys to support transportation, reviewed license requirements, and discussed preparation with cognizant Exelon personnel. The inspector also reviewed personnel training relative to NRC Bulletin 79-19 and 49 CFR 172, Subpart H. The inspector reviewed and discussed technical training presented to workers. The inspector verified that a training program was provided to personnel responsible for the conduct of radioactive waste processing and radioactive waste shipping activities.

b. Findings

No findings of significance were identified.

.5 Shipment Records and Documentation

a. Inspection Scope

The inspector selected and reviewed the records associated with six non-exceptedshipments of radioactive material made since the previous inspection in this area (Shipment Nos. PM-07-057, PW-07-010, PW-06-030, PW-07-007, PW-07-001, PW-07-003). The shipments were selected based on waste classification and waste-stream characteristics. The following aspects of the radioactive waste, radioactive material packaging, and radioactive material shipping activities were reviewed:*Implementation of applicable shipping requirements including completion of waste manifests;*Implementation of the specifications in applicable Certificates of Compliance, asappropriate, for the approved shipping casks including limits on package contents;*Classification and characterization of waste relative to 10 CFR 61.55 and 61.56, asappropriate;*Implementation of up-to-date NRC and Department of Transportation (DOT)shipping requirements;*Implementation of 10 CFR 20, Appendix G;

  • Implementation of specific radioactive material shipping requirements;
  • Packaging of shipments;
  • Labeling of shipping containers;
  • Placarding of transport vehicles;
  • Conduct of vehicle checks;
  • Provision of driver exclusive use and emergency instructions, as applicable;
  • Completion of shipping paper/disposal manifest;
  • Evaluation of package against package performance standards, as appropriate;
  • Conformance with procedures for cask loading, closure and use requirementsincluding consistency with cask vendor approved procedures; and*Use of latest revision documents.

13EnclosureThe review was against criteria contained in 10 CFR 20; 10 CFR 61; 10 CFR 71;applicable DOT requirements, as contained in 49 CFR 170-189 for the above areas; station procedures; applicable disposal facility licenses; and applicable Certificates ofCompliance or vendor procedures for various shipping casks.The inspector also selectively reviewed the 2006 Annual Radioactive Effluent ReleaseReport, relative to types and quantities of radioactive waste shipped offsite and relative to changes to the PCP.

b. Findings

No findings of significance were identified..6 Audits and Assessments of Radioactive Waste Handling

a. Inspection Scope

The inspector reviewed audits and assessments of the radioactive waste handling,processing, storage, and shipping programs, including the PCP. The inspector also reviewed selected corrective action documents written since the previous inspection. The following documents were reviewed:*Chemistry, Radwaste, and Process Control Audit, (NOSA-PEA-06-04 (IR 476157),May 3, 2006; *Self-Assessment, ASSA-565928 A05, May 14, 2007; and

  • Issue Reports (IRs) 632879, 626897, 626873, 618653, 612012, 605803,592478486694, 240959, 642483, 642097, 642491, 632526, 486694. The review was against criteria contained in 10 CFR 20 Appendix G, 10 CFR 71.101, andapplicable station audit and surveillance procedures.

b. Findings

No findings of significance were identified.4.OTHER ACTIVITIESCornerstones: Barrier Integrity & Emergency Preparedness 4OA1Performance Indicator (PI) Verification (71151 - 7 Samples)

.1 Barrier Integrity PIs ( 71151 - 4 Samples)

a. Inspection Scope

The inspectors reviewed a sample of PBAPS's submittals for the four Barrier Integrity PIslisted below to verify the accuracy of the data reported. The PI definitions and the guidance contained in Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment Indicator Guideline," Revision 4, and Exelon procedure LS-AA-2001, "Collecting and 14EnclosureReporting of NRC Performance Indicator Data," were used to verify that the reportingrequirements were met. The inspectors reviewed raw PI data collected since January 2006 to December 2006 and compared graphical representations from the most recent PI report to the raw data to verify the data was included in the report. The PIs reviewed were:*Unit 2 and Unit 3 RCS Specific Activity; and*Unit 2 and Unit 3 RCS Leakage.

b. Findings

No findings of significance were identified..2Emergency Preparedness (EP) PIs (71151 - 3 Samples)

a. Inspection Scope

The inspectors reviewed data for the following EP PIs:

  • Drill and Exercise Performance (DEP);*ERO Drill Participation; and
  • ANS Reliability. The inspectors reviewed supporting documentation from drills and tests from April 2006through March 2007, to verify the accuracy of the reported data. The review of these PIs was conducted in accordance with NRC IP 71151. The acceptance criteria used for the review were 10 CFR 50.9 and NEI 99-02, Revision 4, "Regulatory Assessment Performance Indicator Guidelines."

b. Findings

No findings of significance were identified.4OA2Identification and Resolution of Problems (71152 - 1 Sample)

.1 Routine Review of Items Entered Into the CAP

a. Inspection Scope

As required by IP 71152, "Identification and Resolution of Problems," and in order to helpidentify repetitive equipment failures, human performance issues or program issues for follow-up, the inspectors performed routine screening of issues entered into PBAPS's CAP. This review was accomplished by selectively reviewing copies of IRs and accessing PBAPS's computerized database.

b. Findings

No findings of significance were identified.

15Enclosure.2Review of Operator Work-Arounds (OWAs) (71152 - 1 Work-Around Sample)

a. Inspection Scope

As required by IP 71152, "Identification and Resolution of Problems," the inspectorsconducted a review of the OWA program to verify that PBAPS was identifying OWAs problems at an appropriate threshold, have entered them in the CAP, and proposed or implemented appropriate corrective actions. The inspectors reviewed the list of OWAs and operator challenges (OCs) identified and managed in accordance with Exelon procedure, OP-AA-102-103, "Operator Work-Around Program." Specifically, the review was conducted to determine if any OWAs for mitigating systems affected the mitigating system's safety functions or affected the operator's ability to implement abnormal and emergency operating procedures. The inspectors reviewed the following open OWAs being tracked by PBAPS:*Unit 3 Steam Jet-Air Ejector (SJAE) Suction Valves Fail to Open When Placing theSJAE In-Service (Action Request (AR) A1536806).The inspectors also reviewed the lists of open OCs (deficiencies that are obstacles tonormal plant operations), periodically walked down the panels in the main control room, and reviewed control room deficiencies to identify and be cognizant of:

(1) OWAs that have not been evaluated by PBAPS, and
(2) OWAs that increase the potential for personnel error, including OWAs that: *Require operations contrary to past training or require more detailed knowledge ofthe system than routinely provided; *Require a change from longstanding operational practices;
  • Require operation of a system or component in a manner dissimilar from similarsystems or components;*Create the potential for the compensatory action to be performed on equipment orunder conditions for which it is not appropriate;*Impair access to required indications, increase dependence on oralcommunications, or require actions under adverse environmental conditions; and*Require the use of equipment and interfaces that had not been designed withconsideration of the task being performed.

b. Findings

No findings of significance were identified..3Semi-Annual Review to Identify Trends (71152 - 1 Semi-annual Trend Sample) .aInspection ScopeAs required by IP 71152, Identification and Resolution of Problems, the inspectorsreviewed a list of approximately 5,000 IRs that Exelon initiated at PBAPS from December 1, 2006 through June 1, 2007, to perform the semi-annual PI&R trend review.

Approximately, 30 IRs were reviewed in detail to verify that the issues were adequately identified, appropriately evaluated and corrected. The inspectors review was focused on 16Enclosurehuman performance issues. The review also included issues documented within PBAPS'sStation Trend Review for the fourth quarter of 2006 and the first quarter of 2007.

b.Assessments and ObservationsAlthough no findings of significance were identified, the inspectors observed that the plantis being challenged by human performance deficiencies. Specifically, procedure adherence was the aspect of human performance that was most frequently challenged.

Examples are documented in IRs 568038, 577381, 581258, 604364, 596616, 626534 and 633532. Procedure quality was another aspect of human performance that was challenged. Examples are documented in IRs 635028, 633532, and 600686. However, the inspectors did not identify any new trends that were not previously identified by PBAPS under their quarterly Station Trend Review reports. The inspectors noted that the Station Trend Review report had identified procedure adherence issues as an emerging trend. The inspectors also noted that improving human performance was identified as one of five Station Focus areas for 2007.4OA3Event Followup (71153 - 5 Samples)

.1 (Closed) Unresolved Item (URI)05000277/2007002-04, Incorrect Size Breaker Resultedin a Fire in the '4T4' 480 Volt Load Center

a. Inspection Scope

URI 05000277/2007002-04 was opened in NRC Inspection Report 050000277;05000278/2007002. PBAPS had preliminarily determined that the fire resulted from an apparent mismatch between the ratings of one breaker and its cubicle in the '4T4' 480 volt load center. PBAPS's report also documented that operators responded to the equipment losses caused by the fire by initiating a transient of controlled reactor power reductions to stabilize the plant at approximately 50 percent of rated power. The URI was opened pending the NRC staffs' characterization of this issue following review of PBAPS's causal evaluation and corrective actions. PBAPS's root cause report (RCR) and the associated IR 596616 for this event were reviewed to assess the identified issues. The characterization of this issue as a finding and its risk significance are discussed below.

This URI is closed.

b. Findings

Introduction.

A Green self-revealing finding was identified for inadequate implementationof WO instructions to verify the correct breaker frame size during the overhaul of a compatible spare breaker for installation into the '4T4' 480 volt load center. This condition resulted in a poor electrical connection between the primary disconnect fingers and the switchgear bus stabs for one breaker in the '4T4' load center that ultimately resulted in a fire that led to a plant transient and declaration of an Unusual Event (UE).Description. On February 27, 2007, operators reduced Unit 3 reactor power from 100percent to 50 percent RTP in response to the effects of a fire in the '4T4' 480 volt load center. PBAPS's RCR stated that the fire was caused by an electrical fault in one breaker cubicle that occurred due to a poor electrical connection between the breaker primary 17Enclosuredisconnect fingers and the switchgear bus stabs. This poor electrical connection resultedfrom a configuration error that placed the wrong frame size breaker into the cubicle in the

'4T4' 480 volt load center creating a high resistance, high temperature connection.

The RCR identified that a root cause for the configuration error was that standards,policies, and administrative controls (SPAC) were not used. Specifically, SPAC were notused, in that, the maintenance technicians did not strictly adhere to WO instructions to specifically verify the frame size during the overhaul of a spare breaker that was intended to be placed into the breaker cubicle. The inspectors determined that this issue was a performance deficiency becausemaintenance technicians did not follow WO instructions to verify the correct breaker frame size during the overhaul of a spare breaker.

Analysis.

This finding is greater than minor because it affected the human performanceattribute of the Initiating Event Cornerstone, in that, the incorrect frame size breaker was installed in cubicle for which it was not sized. This mismatch caused an electrical fault that led to a fire and a transient that upset plant stability.

The inspectors evaluated the finding in accordance with IMC 0609, Appendix A, "SDP ofReactor Inspection Findings for At-Power Situations." The SDP Phase 1 screeningidentified that the finding was of very low safety significance (Green) because it did not increase both the likelihood of a reactor scram and that mitigation equipment or functions would not be available. The inspectors determined that this finding had a cross-cutting aspect in the area ofhuman performance (work practices component) because maintenance technicians did not follow WO instructions to specifically verify the frame size of a breaker during its overhaul (IMC 0305 aspect H.4(b)).

Enforcement.

The inspectors determined that the finding did not represent a violation ofregulatory requirements because it involved the '4T4' 480 volt load center, a non-safety related electrical bus. This finding will be tracked as FIN 05000278/2007003-01, Inadequate Implementation of Work Order Instructions Caused the Installation of an Incorrect Size Breaker and Resulted in a Fire in the '4T4' 480 Volt Load Center.2(Closed) URI 05000277/2007002-05, Missed Procedure Step Resulted in UnplannedOverloading of the E-3 EDGURI 05000277/2007002-05 was opened in NRC Inspection Report 050000277;05000278/2007002, pending the NRC staffs' characterization of this issue following a review of PBAPS's root cause analyses, corrective actions taken or planned, approved procedures, and other documents. The characterization of this issue as a finding and its risk significance are discussed below. This URI is closed.

b. Findings

Introduction.

A self-revealing (Green) NCV of Technical Specification (TS) 5.4.1, wasidentified when operators inadequately implemented a surveillance test by missing a 18Enclosureprocedure step. The missed step placed the E-3 EDG in the isochronous mode ofoperation while it was synchronized to off-site power and resulted in an unexpected over-loading of the E-3 EDG.

Description.

During the conduct of a E-3 EDG ST on March 15, 2007, a licensed operatormissed the performance of a required step in a supporting system operating (SO)procedure. The omission of the procedure step placed the E-3 EDG in the isochronous mode while synchronized with off-site power through a 4 kilovolt (kV) vital bus. This condition resulted in unexpectedly loading the E-3 EDG beyond its 30-minute load rating.

The ST-O-052-123-2, "E3 Diesel Generator RHR Pump Reject Test," and the supporting SO 52.A.1.B, "Diesel Generator Operations," directed the synchronization of the E-3 EDG, in the droop mode, to a selected 4 kV bus to pick up the bus loads. The SO 52.A.1.B procedure subsequently directed opening the off-site power feeder breaker to the 4 kV vital bus (the missed step) before placing the EDG in the isochronous mode in accordance with ST-O-052-123-2. The inspectors reviewed PBAPS's root cause investigation report (IR 604364) tounderstand the underlying causes for this event. The inspectors noted that PBAPS identified two root causes for this self-revealing event. First, the plant reactor operator (PRO) did not adhere to the requirements of HU-AA-104-101, "Procedure Use and Adherence" for "Level 1 - Continuous Use," procedures which requires that each procedure step be read prior to being performed, performing each step in the sequence specified, and signing off each step as complete prior to proceeding to the next step.

Specifically, procedure adherence broke down because the PRO allowed himself to be distracted and lost his place in SO 52.A.1.B. Therefore, the off-site feeder breaker to the E-33 bus was not opened in accordance with the SO prior to transferring the E-3 EDG to the isochronous load control mode per the ST.The second root cause for this event was inadequate supervisory oversight during acritical transition between the ST and SO procedures. Specifically, the peer checker and the control room supervisor were not directly observing the operation of the E-3 EDG at the main control room panel during the critical transition between procedures. The transition between procedures should have been identified as a critical step in the testing evolution. This breakdown in crew teamwork resulted in the PRO performing a critical step, without direct oversight, during an infrequently performed test of safety-related equipment. As a result, no one challenged the PRO's decision to transfer the E-3 EDG to the isochronous load control mode when system conditions did not support it.Based on the above, the inspectors determined that inadequately implementing asurveillance test by missing a procedure step was a performance deficiency.

Analysis.

The inspectors concluded the finding was more than minor because it wasassociated with the human performance attribute of the Mitigating Systems Cornerstone, and impacted the cornerstone objective of ensuring the availability of E-3 EDG to respond to initiating events, in that, after the EDG was overloaded, additional unavailability was incurred to inspect the EDG for damage before it was returned to service. The E-3 EDG was inoperable for an additional 46 hours5.324074e-4 days <br />0.0128 hours <br />7.60582e-5 weeks <br />1.7503e-5 months <br /> and was unavailable for an additional 12.5hours. Traditional enforcement does not apply since there were no actual safety 19Enclosureconsequences or potential for impacting the NRC's regulatory function, and the findingwas not the result of any willful violation of NRC requirements.

The inspectors completed a significance determination of this issue using IMC 0609,"SDP," Appendix A, "Determining the Significance of Reactor Inspection Findings for At-Power Situations." The inspectors concluded that this finding affected the Mitigating Systems Cornerstone and answered "No" to all relevant questions. Specifically, all other EDGs remained operable and the actual loss of safety function for E-3 EDG was shorter than its TS allowed outage time of seven days. Therefore, this finding was considered to be of very low safety significance (Green).The inspectors determined that this finding had a cross-cutting aspect in the area ofhuman performance (work practices component) because PBAPS personnel did not follow procedures when the E-3 EDG was placed in the isochronous load control mode with the E-3 EDG in parallel with the off-site power source. (IMC 0305 aspect H.4(b))Enforcement. TS 5.4.1 requires that procedures be implemented covering the activities inRegulatory Guide (RG) 1.33. RG 1.33, Appendix A, Section H.2.b requires that surveillance procedures be developed for testing EDGs.

Applicable ST-O-052-123-2, Step 6.3.1, instructed the operators to synchronize and load the E-3 EDG to the 4 kV bus being tested in accordance with SO 52A.1.B. Step 4.4.16 of SO 52A.1.B directed the operators to open the off-site power source feeder breaker to the E-33 bus before placing the EDG controls in the isochronous load control mode. Contrary to the above, on March 15, 2007, operators missed SO 52A.1.B, Step 4.4.16,and did not open the applicable off-site power breaker before returning to ST-O-052-123-2, Step 6.3.2. Therefore, when the PRO placed the E-3 EDG in the isochronous load control mode in Step 6.3.2, there was an unexpected increase in E-3 EDG load and a trip of the E-3 EDG output breaker.PBAPS placed this issue in the CAP by initiating IR 604364. The corrective actions forthis event included: 1) the selective implementation of additional peer checking of procedure performance place-keeping; and, 2) the E-3 EDG was inspected for potential damage and tested before being returned to an operable status on March 17, 2007.

Because this violation was of very low safety significance (Green) and documented in PBAPS's CAP as IR 604364, this finding is being treated as an NCV, consistent withSection VI.A of the NRC Enforcement Policy: NCV 05000277/2007003-02;05000278/2007003-02, Missed Procedure Step Resulted in Unplanned Overloading of the E-3 EDG

..3Personnel Performance - Failure of DDFP

a. Inspection Scope

The inspectors reviewed corrective action documents listed in the Attachment to thisreport, and discussed the events surrounding the failure of the DDFP with the site fire protection engineer. The inspectors reviewed Revisions 10 and 12 of ST-O-37D-340-2, "DDFP Flow Rate Test," and Revision 2 of NOM-C-7.1, "Procedure Use."

b. Findings

Introduction.

A self-revealing Green NCV was identified for failure to comply with TS5.4.1, "Procedures," which required that procedures be established, implemented, and maintained for the Fire Protection Program.

Description.

PBAPS TS 5.4.1.a, requires that procedures be established, implementedand maintained as recommended in Appendix A to RG 1.33, dated November 1972.

RG 1.33, Appendix A, Section 1, "Administrative Procedures," includes the fire protection program. The Nuclear Operations Manual (NOM)-C-7.1, "Procedure Use," requires that procedures be used for any task which has the potential to cause a system or component to become inoperable.On May 23, 2007, during performance of ST-O-37D-340-2, the DDFP was declaredinoperable due to low discharge pressure. After running the DDFP, the procedure directed cleaning of the cooling water strainer, but did not provide specific instructions on how to perform this task. Without procedure guidance or instructions, operations personnel performing the DDFP test closed an upstream hand valve to isolate the strainer for cleaning. After reassembling the strainer, the operations personnel did not re-open the hand valve. The cooling water was not properly realigned for service because equipment manipulations were performed outside of procedure guidance. On May 24, 2007, ST-O-37D-340-2 was re-performed with the cooling water supply isolated. The engine was damaged during operation without cooling water as a result of the valve mis-alignment. The DDFP was subsequently returned to service on May 30, 2007, following repairs. Additionally, the DDFP flow rate test procedure was revised to include specific instructions for cleaning the cooling water strainer. The procedure was also revised to include instructions for monitoring the engine cooling water and lubricating oil parameters during engine operation. Based on the above, the inspectors determined that manipulating the DDFP cooling watervalve without procedure guidance was a performance deficiency.

Analysis.

The inspectors concluded that the failure to use a procedure for cleaning andrestoring the DDFP cooling water strainer was a more than minor finding because it was associated with the degradation of a fire protection feature, in that, the DDFP was rendered inoperable by damage to the engine. Traditional enforcement does not apply since there were no actual safety consequences or potential for impacting the NRC's regulatory function, and the finding was not the result of any willful violation of NRC requirements.

The inspectors assessed the finding using the Fire Protection SDP (Appendix F to IMC 0609) and determined the finding to be of very low safety significance (Green). The finding was of low significance due to the motor-driven fire pump remaining operable during the five days the DDFP was inoperable, and the small number of fire scenarios which would impact the power supply to the motor-driven fire pump.

21EnclosureThe inspectors determined that this finding had a cross-cutting aspect in the area ofhuman performance (resources component) because procedure ST-O-37D-340-2 did not provide complete and accurate instructions for cleaning the DDFP cooling water strainer.

(IMC 0305 aspect H.2©)Enforcement. TS 5.4.1.a and NOM-C-7.1 require that procedures be used for equipmentmanipulations which could cause fire protection components to become inoperable.

Contrary to the above, procedures were not used when manipulating the DDFP cooling water isolation valves on May 23, 2007, resulting in the DDFP being run on May 24, 2007, without cooling water and sustaining engine damage. Because this failure to comply with TS 5.4.1.a is of very low safety significance (Green) and has been entered into PBAPS's CAP as IR 633532, this violation is being treated as an NCV, consistent with Section VI.Aof the NRC Enforcement Policy: NCV 05000277, 278/2007003-03, InadequateProcedure Adherence Results in Damage to the DDFP

..4(Closed) Licensee Event Report (LER) 05000277/2006002-00, AutomaticDepressurization System (ADS) SRV DeficienciesOn September 28, 2006, engineering personnel determined that the 71B and 71G SRVsdid not meet their allowable leak rate for the pneumatic actuation controls for the ADS feature of the SRVs. Additionally, the 71C SRV, Serial Number 9S/N 83, did not properly re-close on the fourth actuation during laboratory testing. The cause of the 71B and 71G ADS SRV pneumatic leakage is attributed to leakage from each of the SRV's actuator diaphragm and solenoid valve. These leaks only occurred when the SRV solenoid valveswere energized. The diaphragms and solenoid valves associated with the 71B and 71G ADS SRVs were replaced under work orders C0219044 and C0219034. As-left leak testing was performed and the values were restored to an operable condition prior to plant startup from the P2R16 Refueling Outage. A refurbished SRV was installed in the 71C SRV location to replace the S/N 83 SRV. The corrective actions to resolve the underlying causes of this event are in the CAP (IR 539277). This licensee-identified violation was more than minor since it was associated with theEquipment Performance attribute of the Mitigating Systems Cornerstone and impacts the cornerstone objective of ensuring the reliability, availability, and capability of systems that respond to initiating events, in that, if the ADS system was called upon to actuate it's operability would not be ensured. The inspectors evaluated this finding using IMC 0609, Appendix A, "SDP of Reactor Inspector Findings for At-Power Situations," Phase 1 screening. Specifically, using the Mitigating Systems Cornerstone column, the inspectors determined that a Phase 2 evaluation was required because the finding represented a loss of system safety function. The inspectors concluded that the finding was of very low safety significance (Green) because the success criteria for depressurization, on each of the applicable worksheets, only required the use of 2 of 11 SRVs. A regional senior reactor analyst reviewed and concurred with the inspectors risk assessment. This licensee-identified finding involved a violation of TS 3.5.1, "Emergency Core Cooling Systems." The enforcement aspects of this violation are discussed in Section

4OA7 of

this report. This LER is closed.

22Enclosure.5(Closed) LER 05000277/2006004-00, Plant Modification Created Diesel GeneratorBuilding Carbon Dioxide Suppression Room Flooding VulnerabilityOn November 17, 2006, engineering personnel determined that a potential floodvulnerability had existed in the EDG building carbon dioxide suppression room. A plant modification performed in 1985 had installed a catch basin at the EDG building fuel oil filling station, which is located outside the EDG building. The catch basin discharge was tied into the EDG building's oily waste separator tank, upstream of the flood protection isolation valve. This constituted an unanalyzed condition that degraded plant safety. In the event of a design basis flood, a potential pathway existed for flood water to enter the building through the floor drains. It was determined that the maximum credible flow rate would have exceeded the capability of the floor drain sump and sump pumps. Under design basis flood conditions, the ESW system booster pumps and return valves, and the HPSW system return valves would be challenged to perform their safety function.

Corrective actions recommended for this issue were documented in IR 554800 and included revision of the applicable special event procedure for floods to mitigate this condition. This finding is more than minor because it was associated with a degraded condition thatcould concurrently influence mitigation equipment. Specifically, with the degraded flood barrier for the EDG building carbon dioxide suppression room, the ESW system booster pumps and return valves and the HPSW system return valves would be challenged to perform their safety function under design basis flood conditions. The NRC IMC 0609, Appendix G, "Shutdown Operations SDP," applies because the plant would be shutdown, at 112', in accordance with plant procedures, before flooding of EDG building would begin to occur at the 128' elevation, as noted in the LER. Also, as noted in the LER, the design basis flood would be expected to reach the 132' elevation. A Phase 1 SDP was performed using Checklist 5 of IMC 0609, Appendix G, Attachment 1. The inspectors determined that a Phase 2 or 3 SDP was required because the finding:*Increased the likelihood that a loss of decay heat removal will occur due to afailure of its support systems; *Would degrade the ability to cope with a loss of offsite power; and

  • Would degrade the ability to establish an alternate core cooling path if decay heatremoval cannot be re-established for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The inspectors determined that the finding was of very low safety significance (Green)because of: the very low likelihood of occurrence of a design basis flood reaching the 132' elevation; flood alarms in the EDG building carbon dioxide suppression room that would enable operators to take actions to stop the flooding; or operators could manually operate the service water system return valves. A regional senior resident analyst reviewed and concurred with the inspectors risk assessment. This licensee-identified finding regarding the installation of a modification that placed the station in an unanalyzed condition involved a violation of 10 CFR 50.59. The enforcement aspects of this violation are discussed in Section

4OA7 of this report.

23Enclosure4OA5Other ActivitiesAs a plant status activity, the inspectors used guidance in NRC IP 60855.1, "Operation ofan Independent Spent Fuel Storage Installation at Operating Plants," to selectively verify that PBAPS performed dry cask loading in a safe manner and in compliance with approved procedures and work order instructions.4OA6Meetings, Including Exit.1Exit Meeting SummaryOn July 20, 2007, the resident inspectors presented the inspection results to Mr. J. Grimes and other PBAPS staff, who acknowledged the findings. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary. No proprietary information was identified.

.2 Annual Assessment MeetingOn April 4, 2007, Mr. Paul Krohn, Mr. Mel Gray, the resident inspection staff, and otherNRC staff held a public meeting with Mr. Joe Grimes and other PBAPS staff, to discuss

the results of the NRC's assessment of performance at PBAPS for the period January 1, 2006 through December 31, 2006. The handouts from the meeting are available electronically from the NRC's document system (ADAMS) under accession number ML071000066. Following the meeting, the NRC staff held a session to accept public comments and respond to public questions.4OA7Licensee-Identified ViolationsThe following violations of very low safety significance (Green) were identified by thelicensee and are violations of NRC requirements which meet the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as NCVs.*10 CFR 50.54(q) requires that the licensee shall follow and maintain in effectemergency plans which meet the standards in 50.47(b) and the requirements in Appendix E. The Exelon Nuclear Standardized Radiological Emergency Plan forPeach Bottom, Part II, Section E.2 b.1 states for State/Local Agencies: A notification shall be made within fifteen

(15) minutes of the initial emergency classification. Contrary to this, on February 27, 2007, during an emergency event, Peach Bottom personnel failed to notify one local county within 15 minutes of an initial emergency declaration (Unusual Event); the notifications were completed in 18 minutes. The notification was not made in a timely manner because the primary phone link to the county was not available. Plant procedures require the notifications to be made using a backup phone. This finding is of very low safety significance (Green) because the notification was late by only 3 minutes, backup communication equipment was available, and procedures were available to use the backup communication equipment. This was entered in PBAPS's CAP as IR

596641.

24Enclosure*10 CFR 50.59, "Changes, Tests, and Experiments," requires, in part, that thelicensee may make changes in the facility as described in the safety analysis report without prior Commission approval, unless the proposed change involves a change in the TSs incorporated in the license or an unreviewed safety question (USQ). A proposed change shall be deemed to involve a USQ, in part, if the consequences of an accident or a malfunction of equipment important to safety previously evaluated in the safety analysis report may be increased. Contrary to this, in 1985, a change to the facility was made that remained in place until November 2006, without analyzing whether a USQ existed. Specifically, as documented in Section 4OA3.5, a plant modification performed in 1985 introduced a potential flood vulnerability for the EDG building carbon dioxide suppression room. The flood vulnerability posed by this change constituted an unanalyzed condition that degraded plant safety. This was identified in PBAPS's CAP as IR 554800. This finding is of very low safety significance (Green) because the likelihood of a design basis flood that could affect mitigation equipment is very small and manual operator action could be taken to mitigate the effects of a design basis flood.*TS 3.5.1, "Emergency Core Cooling Systems," requires that the ADS function offive SRVs be operable. TS 3.5.1, Action H, requires the plant to be brought to Mode 3 in 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> if two or more SRVs are inoperable. Contrary to the above, on September 28, 2006, the pneumatic actuation controls for the ADS function of two SRVs (71B and 71G) did not meet their allowable leak rate acceptance criteria.

Specifically, the as-found leak rates for the 71B and 71G SRVs were documented as off-scale and were in excess of the allowable the leak rate limit of 100 cc/min.

Unit 2 was shutdown and in a refueling outage when the event was discovered.

However, Unit 2 had been operating for the previous 367 days. This issue was entered in PBAPS's CAP as IR 539277. As documented in Section 4OA3.4, a Phase 2 SDP determined that the finding was of very low safety significance (Green) because the success criteria for depressurization, on each of the applicable SDP notebook worksheets, only required the use of 2 of 11 SRVs.ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Exelon Generation Company Personnel

J. Grimes, Site Vice President
M. Massaro, Plant Manager
N. Alexakos, Manager, Engineering-Programs
J. Armstrong, Regulatory Assurance Manager
C. Behrend, Engineering Director
G. Jardel, Manager, Emergency Preparedness
C. Jordan, Chemistry Manager
D. Lewis, Operations Director
H. McCrory, Radiation Protection Technical Support Manager
M. Ross, Radwaste, Environmental Supervisor
G. Stathes, Maintenance Director
S. Taylor, Manager, Radiation Protection
T. Van Wyen, Operations Training Manager
A. Wasong, Training Director

NRC Personnel

F. Bower, Senior Resident Inspector
M. Brown, Resident Inspector
R. Fuhrmeister, Senior Project Engineer
R. Nimitz, Senior Health Physicist
N. Perry, Sr. Emergency Response Coordinator
R. Cureton, Emergency Preparedness Inspector

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened None.Opened and

Closed

05000278/FIN-2007003-01FINInadequate Implementation of WOInstructions Caused the Installation of

an Incorrect Size Breaker and

Resulted in a Fire in the '4T4' 480 Volt
Load Center (Section 4OA3.1)05000277, 278/2007003-02NCVMissed Procedure Step Resulted inUnplanned Overloading of the E-3
EDG (Section 4OA3.2)
A-2Attachment05000277, 278/2007003-03NCVInadequate Procedure AdherenceResults in Damage to the DDFP

(Section 4OA3.3)

Closed

05000278/FIN-2007003-01FINInadequate Implementation of WOInstructions Caused the Installation of

an Incorrect Size Breaker and

Resulted in a Fire in the '4T4' 480 Volt
Load Center (Section 4OA3.1)05000277, 278/2007003-02NCVMissed Procedure Step Resulted inUnplanned Overloading of the E-3
EDG (Section 4OA3.2)
A-2Attachment05000277, 278/2007003-03NCVInadequate Procedure AdherenceResults in Damage to the DDFP

(Section 4OA3.3)

Discussed

None.

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse WeatherWC-AA-107, Revision 4, Seasonal ReadinessOP-AA-108-111-1001, Revision 2, Severe Weather and Natural Disaster Guidelines

OP-PB-108-111-1001, Revision 3, Preparation for Severe Weather
RT-O-040-610-2, Revision 12, Outbuilding HVAC and Equipment Inspection for SummerOperationSO 52A.1.B, Revision 39, Diesel Generator Operations

Section 1R04: Equipment AlignmentCOL 52A.1.A-3, Revision 12,

E-3 Diesel Generator Normal StandbySO 53.7.A - App 1, Revision 0, Removal of 220-08 Line from Service
COL 13.1.A-2, Revision 19, RCIC System
COL 33.1.A-2, Revision 20, ESW System (Unit 2 and Common)
COL 32.1.A-2, Revision 10, HPSW System
SO 32.1.A-2, Revision 12, HPSW System Startup and Normal Operatoins
A-3AttachmentP&ID DiagramM-315 Sheet 1, Revision 64, ESW and HPSW SystemsM-315 Sheet 4, Revision 53, ESW and HPSW Systems
M-315, Sheet 1, Revision 65, ESW and HPSWSystemsM-330, Sheet 1, Revision 35, Emergency Cooling System
M-361, Sheet1, Revision 80, RHR System
M-361, Sheet 2, Revision 67, RHR System

Section 1R05: Fire ProtectionPF-63, Revision 1, Prefire Strategy Plan Unit 3 Reactor Bldg.

RCIC Room, 88' ElevationPF-70, Revision 2, Prefire Strategy Plan Standby Gas Treatment Room, Radwaste Building,91' 6" ElevationPF-13H, Revision 3, Prefire Strategy Plan North CRS Equipment and West Corridor, Unit 3Reactor Building, 135' ElevationPF-55, Revision 3, Prefire Strategy Plan, Fire Zone 55, Unit 3 Refuel Floor, Reactor Building,234' ElevationPF-13D, Revision 1, Prefire Strategy Plan 3 'A' & 3 'C' Core Spray Rooms, Reactor Building,91'6" Elevation, Fire Zones 13D & 13EPF-60, Revision 1, Prefire Strategy Plan, Unit 2 Reactor Building RCIC Room, 88' Elevation
PF-127, Revision 4, Prefire Strategy Plan, Unit 2 Emergency Battery/ Switchgear Room andRadwaste Corridor,
TB-135PF-132, Revision 4, Prefire Strategy Plan, Diesel Generator Building, Elevation 127', Fire Zone 132PF-151, Revision 3, Prefire Strategy Plan, Unit 2 Main Transformer Yard, Fire Zone 151
PF-164, Revision 0, Prefire Strategy Plan, 2 Startup Switchgear Building, Fire Zone 164

==Section 1R12: Maintenance EffectivenessIR

607398, Functional Failure of 3AE015 During '4T4' Breaker FireIR
596616, Fault at Unit 3 'B' Iso-Phase Cooler Fan Breaker in 4T4==
IR 614945, Potential Extent of Condition Concern for MCC Bucket Stabs
IR 619579, 480 V Breaker Interference Angle Location Incorrect
IR 617890, Conflicting Data on Cubicle Size of 2 'A' EHC Pump Breaker
IR 599184, Extent of Condition Walkdown of Unit 2 480 V Load Center Bus
IR 606397, Perform ITE Rejection Tab Walkdown
IR 599203, Extent of Condition Walkdown of Unit 3 480 V Load Center Bus
IR 599208, Extent of Condition Walkdown of Common 480 V Load Center Bus
IR 634973, ITE Breaker Found With No Rejection Tab
IR 634971, ITE Breaker Found With No Rejection Tab
IR 634962, ITE Breaker Found With No Rejection Tab
IR 634964, ITE Breaker Found With No Rejection Tab
IR 634966, ITE Breaker Found With No Rejection Tab
IR 634965, ITE Breaker Found With No Rejection Tab
IR 600797, 2007 Buried Pipe Program Inspections
IR 623638, EOC: Generate PM per PCM Template Requirements
IR 623646, EOC: Generate PM per PCM Template Requirements
A-4AttachmentIR
623635, EOC: Generate PM per PCM Template RequirementsIR
603279, Inspect and Clean ESW X-Tie Piping (HV-512A-B) WW 0730
IR 632688, 2 'A' EHC PP Breaker Cubicle Frame Size Incorrect
IR 589654, Potential For Silt Buildup in the ESW Pump Crosstie Piping
ACPS 07-0-002,
HV-0-33-512A, A ESW Pump Discharge Loop X-tie
ST-O-033-300-2, Revision 31, ESW, Valve, Unit Cooler and ECT Functional Inservice Test
ACPS 07-0-002,
HV-0-33-512A, A ESW Pump Discharge Loop X-tie
ST-O-033-300-2, Revision 31, ESW, Valve, Unit Cooler and ECT Functional Inservice Test Performance Monitoring - Unavailability - System 33 (ESW) - Jun 2005 -> Jun 2007
Clearance
07000529, Emergency Cooling Water Pump Discharge Valve
ER-AA-5400, Revision 0, Buried Piping and Raw Water Corrosion Program Guide
ER-AA-5300, Revision 0, Raw Water Corrosion Program Guide
ER-AA-5400-1002, Revision 0, Buried Piping Examination GuideSection 1R13: Maintenance Risk Assessments and Emergent Work ControlWC-AA-101, "On-line Work Control Process"Adverse Condition Monitoring and Contingency Plan (CAMP), 3 'A' Recirculation Pump Seal Unstable Second Stage Seal Temperature and Increasing Second Stage Seal Pressure, Dated 04/17/2007AR A1612541, Rising 3 'A' Recirculation Pump #2 Seal Temperature
AR A1610537, High Lube Oil Temperature Alarm During E-2 EDG Run
AR A1613094-01, Technical Evaluation: CRD Suction Source Swap from Condensate to Unit 3 CSTIR
623723, Bolt and Heli-coil Found Damaged at Disassembly on 00T634
SF-220, Revision 21, Spent Fuel Cask Loading and Transport Operations
A1406063, Review of Mod 79-028 Recirculation Seal Pressure Bleed Off
EC 360901, Exelon Fleet Reactor Recirculation Pump Seal Condition Monitoring TemplateIR
620785, Continuous Venting of the Recirculation Seals not EvaluatedAO 2A.16-3, Revision 2, Manual Adjustment of Recirculation Pump Seal Second Stage PressureSO 2A.1.C-3, Revision 10, Operation of the Recirculation Pump Seal Purge System
A1439223, 3AP034: Seal Hi Temp Alarm & Hi 2

nd Stage PressureACMP - Unit 3, 3 'B' Recirculation Pump Seal Increasing Second Stage Seal Pressure

A1613202, 3 'B' Recirculation Pump 2

nd Stage Seal PressureIR

619609, 3 'B' Recirculation Pump 2

nd Stage Seal PressureARC 30C204M A-1, Revision 4 - A Recirculation Pump Seal Stage 2 Hi Flow

ARC 30C204M A-2, Revision 6 - A Recirculation Pump Seal Stage 2 Lo Flow
OP-PB-108-101-1002, "Guidelines for Control of Protected Equipment," Revision 4
WC-AA-101, "On-Line Work Control Process," Revision 13
IR 626534, Equipment Not Protected as Required.
IR 624653, Protected Equipment List for 2SUE Outage Incomplete
IR 617946, Protected Equipment List Issued 4/16/07 Initially Incomplete
IR 504032, Exaggerated Paragon List of Protected Equipment
IR 462364-18-04, Paragon Refresher Training
IR 624599, U3 RHR Pump Testing Not Performed per Schedule
IR 634657, PRA Support for Protecting Equipment
IR 474569-17-08, Develop a Tutorial that Help Crews with Paragon
IR 624599, U3 RHR Pump Testing Not Performed per Schedule
IR 644648, Inadequate Guidance in
WC-AA-101 for Protecting Equipment
A-5AttachmentARC-216 20C212L D-1, Revision 5, C Air Comp TroubleSO 36A.7.A-2, Revision 3, Unit 2 'C' Air Compressor Shutdown
ON-119, Revision 14, Loss of Instrument Air
ARC-216 20C212L D-2, Revision 2 Service Air Header Lo Press
ARC-316 20C212L D-2, Revision 1, Service Air Header Lo Press
R1032642, 3CK001 - PM: Perform Annual PM on Compressor
SO 36A.1.A-2, Revision 2, Unit 2 'C' Air Compressor Return-to-Service and Service Air Systems Return to Normal OperationIR
642127, Critique IR on Loss of Service Air to Unit 2 and Unit 3DrawingsP&I Diagram M-356, CRD Rod Drive Hydraulic System Part A, Sheet 2P&I Diagram M-353, Reactor Recirculation Pump System

Section 1R15: Operability EvaluationsIR 615433,

E-4 EDG - 10
CFR 21 Notification for Cam Roller Bushing Material Issue Fairbanks Morse Engine Notification Report Serial Number 06-04, 10
CFR 21 Notification, CamRoller Bushing Incorrect Material, dated April 9, 2007Event Notification Number 43294, Part 21 Notification - Diesel Cam Roller Bushing Failures
IR 388397-04, Prompt Investigation of 3 'A' RRP #2 Seal Cavity Temperature HighAdverse Condition Monitoring and Contingency Plan (CAMP), 3 'A' RRP Unstable Second Stage Seal Temperature and Increasing Second Stage Seal Pressure, dated 04/17/2007Operational and Technical Decision Making (OTDM) No. 07-01, 3 'A' RRP Seal Issues, dated04/17/2007Abnormal Operations (AO) procedure 2A.16-3, Manual Adjustment Recirculation Pump SealSecond Stage PressureOTDM No. 07-02, 3 'A' RRP Seal Temperatures - Re-align CRD Suction Source fromCondensate System to U3 CST, dated 04/20/2007AR A1613094-01, Technical Evaluation:
CRD Suction Source Swap from Condensate to Unit 3 CST PBAPS Technical Requirements Log, Item Number 07-3-080, PTRM 3.6, Function 7, MainSteam Relief Valves, dated May 17, 2007Adverse Condition Monitoring Plan:
DPT-2-02-117DH Sensing Line Leakage, datedMay 24, 2007A1615458, Small Leak on
DPT-2-02-117D Line Snubber Threaded Cap
C0221439, Replace Snubber During an Outage
PB
ECR 03-00326 000, Revise Instrument Rack Drawings with a Note for Snubbers

Section 1R19: Post-Maintenance TestingAR A1610537, High Lube Oil Temperature Alarm During

E-2 EDG RunR1049367, Unit 3
HCU 50-43: HCU Overhaul
ST-R-003-480-3, Average Scram Times for ODYN/B Minimum Critical Power Ratio (MCPR) RequirementsC0216504,
PS-2-13-067-01: Replace Pressure Switch
ST-O-013-301-2, Revision 31, RCIC Pump, Valve, Flow and Unit Cooler Functional andInservice Test, Conducted on April 5, 2007
A-6AttachmentC0215740, 2BG002, Replace EndbellMA-AA-716-230-1002, Revision 1, Vibration Analysis/ Acceptance Guideline
MA-AA-716-230-1003, Revision 1, Thermography Program Guide
SO 60F.1.A-2, Revision 9, Reactor Protection System MG Set and Power Distribution System Startup from Dead Bus ConditionR0629147, 3R4-U-C (7033B), Perform MCU Inspection
A1619582, 3CP343: Pump/Motor Found Seized during Breaker PMT
IR 638369, 3C Glycol Pump found seized during breaker PMT
SO 8G.6.A-3, Revision 3, Placing a Standby Off-Gas Glycol Pump in Service and Placing the InService Pump in Standby or Off

Section 1R22: Surveillance TestingS12T-MIS-8547-C1CQ, Revision 13, Calibration/Functional Check of Channel C Group 1, 4 and 5 of

PCIV Logic for
TSS-80547CST-R-003-485-3, CRD Scram Insertion Timing of Selected Control Rods, Revision 19, completed May 5, 1997

==Section 1R23: Temporary Plant ModificationsIR

618478, Provide Supplemental Cooling to the 3 'A'==
RR Seal Purge LineIR
625092, Equipment Discovered on Floor Hatch H11 in Unit 3 Reactor Building
WO
C0221034, TCCP 07-00172, Install Cooling Unit
AR A1613094, Provide Supplemental Cooling to the 3 'A' RR Seal Purge Line
SP
SO.005-3, Revision 1, Routine Inspection of the 3 'A' Recirculation Seal Purge SupplementalCooling System

Section 1EP2: Alert and Notification System (ANS) EvaluationPeach Bottom Nuclear Power Plant Upgraded Public Alert and Notification Report, April 2005FEMA

ANS Design Report, December 2005EP-MA-121-1002 "Exelon East Alert and Notification System (ANS) Program," Revision 4
EP-MA-121-1004 "Exelon East ANS Corrective Maintenance," Revision 4
EP-MA-121-1005 "Exelon East ANS Preventive Maintenance Program," Revision 3
EP-MA-121-1006 "Exelon East ANS Siren Monitoring, Troubleshooting, and Testing," Revision 5Corrective Maintenance Field Work Instructions for ANS Control Points, Repeaters and Sirens, Approved December 2004Preventative Maintenance Field Work Instructions for ANS Control Points, Repeaters and SirensIRs:
00433494 00565056
00352078
00597065
00481763 00451040
00520830
00521321
00533157 00541478
00596641
A-7Attachment

Section 1EP4: Emergency Action Level (EAL) and Emergency Plan ChangesEP-AA-120-1001 "10

CFR 50.54(q) Change Evaluation," Revision 406-12 "ERO Training and Qualification"
TQ-AA-113, Revision 7
06-16 "Radiological Emergency Plan"
EP-AA-1000, Revision 17
06-33 "EP Plan Administration"
EP-AA-120, Revision 7
06-96 "Emergency Preparedness Advisory Committee"
EP-AA-120-1004, Revision 0
06-97 "Quarterly Satellite Phone Test"
EP-MA-124-1004, Revision 0
06-99 "EP Fundamentals"
EP-AA-1101, Revision 3
06-101"Exelon East ANS Program"
EP-MA-121-1002, Revision 4
06-102"Exelon East ANS Corrective Maintenance Program"
EP-MA-121-1004, Revision 4
06-103"Exelon East ANS Preventative Maintenance Program"
EP-MA-121-1005, Revision 3
06-108"ERO Fundamentals"
EP-AA-1102, Revision 2
06-110"Mid-Atlantic ERO Notification or Augmentation" EP-AA-112-100-F-07
07-11"Exelon East ANS Siren Monitoring, Troubleshooting, and Testing"
EP-MA-121-1006, Revision 407-12"ANS Siren Monthly Test"
RT-E-101-901-2, Revision 8
07-18"Radiological Emergency Plan Annex for PBAPS"
EP-AA-1007, Revision 14
07-39"Exelon East ANS Siren Monitoring, Troubleshooting, and Testing"
EP-MA-121-1006, Revision 5

Section 1EP5: Correction of Emergency Preparedness WeaknessesEP-AA-125 "Emergency Preparedness Self Evaluation Process," Revision4LS-AA-126 "Self-Assessment Program," Revision 5

LS-AA-126-1001 "Focused Area Self-Assessments," Revision 4
Unusual Event Evaluation Reports dated 10/4/06, 11/21/06, 4/16/07
ASSAs:
547869, 565747-04
NOSA:-PEA-06-03 dated 4/13/06
NOSA-PEA-07-04 dated 5/9/07
A-8AttachmentIRs:
00433494
00565056
00352078
00481763
00451040 00520830
00533157
00541478
00596641 00597065
00521321Section 1EP6: Drill EvaluationPeach Bottom Atomic Power Station, May 15, 2007, Off-Year Exercise, Drill ScenarioPeach Bottom Atomic Power Station May 15

th, 2007 Off-Year Exercise Report datedJune 14, 2007IR

630584, Enhancement Opportunity from May 2007 EP Drill
IR 629910, Late State\Local Notification Made During an EP Drill
IR 629970, EAL Classification During Drill Not Timely Quick Human Performance Investigation Report, PB EAL Classification During Drill Not Timely, 05/15/07Quick Human Performance Investigation, Repetitive Issue With Not Completing State/Local Notifications on Time, 5/15/07 Section 2PS2 : Radioactive Material Processing and Transportation10 CFR Part 61 Sampling and Analysis Results (Waste Streams)Radioactive Material Shipping Documentation Radioactive Shipping Container Certifications Audit Template: Chemistry, Radwaste, Effluent and Environmental Monitoring Handling, Storage and Shipping Topical Report, Mobile In-container De-watering and Solidification System
DOT-Type A, Test and Evaluation for Type A Packaging Waste Disposal Facility State Licenses Training Program - DOT/79-19 Training for Support of Radioactive and Asbestos Shipments Training Program - Site Specific Portion of Radioactive Material Shipping Training Program Training Program - Shipper Refresher Type B Cask Handling and Loading Procedures
RT-W-020-980-2, Updating Radwaste Classification Computer Programs
RP-AA-605, 10
CFR 61 Compliance Program
RP-AA-605, 10
CFR 61 Program
RP-PB-605-1001, Peach Bottom 10
CFR 61 Sampling

Section 4OA1: Performance Indicator VerificationLS-AA-2001, Revision 6, Collecting and Reporting of

NRC Performance Indicators DataLS-AA-2090, Revision 4, Monthly Data Elements for NRC RCS Specific Activity
LS-AA-2100, Revision 5, Monthly Data Elements for NRC RCS Leakage
ST-O-020-560-2, Reactor Coolant Leakage Test (sample of completed test records)
ST-O-020-560-3, Reactor Coolant Leakage Test (sample of completed test records)
ST-C-095-864-2, Off Gas Monitor Response and Release Rate Verification by a Grab Sample
A-9AttachmentST-C-095-864-3, Off Gas Monitor Response and Release Rate Verification by a Grab SampleST-C-095-820-2, Determination of Dose Equivalent µCi/g I-131 in Primary Coolant
ST-C-095-820-3, Determination of Dose Equivalent µCi/g I-131 in Primary Coolant
CH-407, Sampling of Reactor Water
CH-C-601, Determination of Dose Equivalent I-131
ERO Drill Participation PI data, April 2006 - March 2007
Public Notification System PI data, April 2006 - March 2007
DEP PI data, April 2006 - March 2007

Section 4OA2: Problem Identification and Resolution577381, Operator Failed to Perform Procedure Step581258, Page 12 of

ST-O-098-01N-2 Discovered Misplaced
568038, SBLC System Inoperable Resulting from Dedicated EO Leaving Area
565945, 4 kV Undervoltage Relay Failure and No IR's Written
569879, 4 kV Undervoltage Relay Failure and No IR's Written
576826, NOS Rated PB OPS Yellow For 4Q06
581376, Test Aborted: "ECT Portable Pump Operability" RT-O-48B-275-2
584506, Through Wall Leak Found on ESW Piping585680, Unit 3 'D' RHR Exceeded the Original Dose Estimate587171,
CHK-0-33-515A Not Seated Causes
ST-0-033-300-2 To Be Aborted
588335, Timeliness/Response to ESW Piping Issue
IR 584506
588800, Weld Verification Deficiency
590373, Trng: FME Training Unexcused Absence
590573, E/S 3-17-477 Power Supply Failed Following Swap of 3 'B' RPS
593883, Unit 2 'C' RHR Sump Overflowed During Heat Exchange Maintenance
593890, Unit 2 'A' RHR Room Spill During Pumping of the Unit 2 'C' Room Sump
593891, Unit 2 'C' RHR Sump Overflowed During Heat Exchanger Maintenance
596641, Unusual Event Notification to York County Was > 15 Minutes
2264, Mid-Cycle Performance Gap - Self Assessment
606458, Training: PIMS Code Improperly Granted
607064, Temperature Recorder
TR-0558 not Functional (Discharge Canal)
615413, Non-Safety-Related Piece Part Installed in Diesel Generator
21191, Inadvertent ERO Activation at PBAPS
23697, Scaffold Taken to Complete in PIMS But Was Not Removed
29910, Late State/Local Notification Made During an EP Drill
29970, EAL Classification During Drill Not Timely
26534, Equipment Not Protected As Required
596616, Fault at 3 'B' Iso-Phase Cooler Fan Breaker in '4T4' Load Center
633532, DDFP/ Engine Trip
604364, Human Error Results in E-3 EDG Overload and E-33 Breaker Trip

Section 4OA3: Event FollowupSpecial Event Procedure (SE)-4, Flood, Revision 21

IR 563253, External Flood Vulnerability - Circulating Water Pump Structure
IR 554800, External Flood Vulnerability Found for EDG Building
IR 520322, E-3 EDG Fire at Roof Exhaust Penetration
A-10AttachmentST-O-37D-370-2, Revision 25, DDFP Operability TestST-O-37D-340-2, Revision 10, DDFP Flow Rate Test
ST-O-37D-340-2, Revision 12, DDFP Flow Rate Test
ST-M-37D-380-2, Revision 3, DDFP Inspection
NOM-C-7.1, Revision 2, Procedure Use
280-E-8, Revision 16, Single line Meter and relay Diagram, Standby Diesel Generators and4160 Volt Emergency Power System, Unit 26280-E-1615, Revision 64, Single Line Meter and relay Diagram, E-124 and E-224 Emergency Load Centers, E-124-R-C and E-224-R-C Reactor Motor Control Centers, and
E-124-T-B and E-224-T-B Turbine Motor Control Centers, 440 Volt, Unit 2Peach Bottom Atomic Power Station Fire Protection Plan, Revision 15
A-11AttachmentIssue ReportsIR 00633037IR 00633453
IR 00633532
IR 00634313IR 00634585IR 00634709
AR 00635028AR 00635257AR 00635267
AR 00635408

LIST OF ACRONYMS

ADAMSAgency-wide Documents Access and Management SystemADSautomatic depressurization system

ANSAlert and Notification System

ARaction request

BTPsbranch technical positions

CAPcorrective action program

CFRCode of Federal Regulations

CRcondition report

CRDcontrol rod drive

CSTcondensate storage tank

DBDsDesign Basis Documents

DDFPdiesel-driven fire pump

DEPDrill and Exercise Performance

DOTDepartment of Transportation

DRPDivision of Reactor Projects

EALemergency action level

EDGemergency diesel generator

EPemergency preparedness

EROemergency response organization

ESWemergency service water

HPCIhigh pressure coolant injection

HPSWhigh pressure service water

HCUhydraulic control unit

IMCInspection Manual Chapter

IPInspection Procedure

IRissue report

kVkilovolt

LERslicensee event reports

MRMaintenance Rule

MSmitigating system

NCVnoncited violation

NEINuclear Energy Institute

NRCNuclear Regulatory Commission

OCsoperator challenges

OWAsoperator work-arounds

PARprotective action recommendation

PARSPublicly Available Records

PBAPSPeach Bottom Atomic Power Station

PCIVprimary containment isolation valve

PCPProcess Control Program

2AttachmentPIperformance indicatorPMTpost-maintenance testing

PROplant reactor operator

RBreactor building

RCICreactor core isolation cooling

RCRroot cause report

RCSreactor coolant system

RFPreactor feed pump

RGRegulatory Guide

RHRresidual heat removal

RRPreactor recirculation pump

RTPrated thermal power

SDPsignificance determination process

SJAEsteam jet-air ejector

SPACstandards, policies, and administrative controls

SOsystem operating

SSCsstructures, systems, and components

SRVsafety relief valve

STssurveillance tests

TRMTechnical Requirements Manual

TRTtroubleshooting, rework and testing

TSTechnical Specification

TSCtechnical support center

UEunusual event

URIunresolved item

UFSARUpdated Final Safety Analysis Report

USQunreviewed safety question

WO work order