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Category:Letter
MONTHYEARIR 05000277/20240032024-11-0404 November 2024 Integrated Inspection Report 05000277/2024003 and 05000278/2024003 RS-24-093, Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-10-10010 October 2024 Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24284A2842024-10-10010 October 2024 (Wcgs), Revision of One Form That Implements the Radiological Emergency Response Plan (RERP) ML24281A1012024-10-0707 October 2024 Senior Reactor and Reactor Operator Initial License Examinations ML24275A2442024-10-0303 October 2024 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief, Division of Operating Reactor Licensing ML24240A1692024-09-18018 September 2024 Cy 2023 Summary of Decommissioning Trust Fund Status ML24221A2582024-09-0606 September 2024 Response to Request for Re-Engagement Regarding the Subsequent License Renewal Environmental Review for Peach Bottom Atomic Power Station, Units 2 and 3 ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification 05000277/LER-2024-003, Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum2024-09-0505 September 2024 Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum IR 05000277/20240052024-08-29029 August 2024 Updated Inspection Plan for Peach Bottom Atomic Power Station, Units 2 and 3 (Report 05000277/2024005 and 05000278/2024005) ML24239A3972024-08-23023 August 2024 Rssc Wire & Cable LLC Dba Marmon - Part 21 Final Notification - 57243-EN 57243 ML24235A0342024-08-23023 August 2024 U.S. Nuclear Regulatory Commission’S Analysis of Constellation Energy Generation’S Decommissioning Funding Status Report IR 05000277/20240102024-08-23023 August 2024 Fire Protection Team Inspection Report 05000277/2024010 and 05000278/2024010 IR 05000277/20240022024-08-14014 August 2024 Integrated Inspection Report 05000277/2024002 and 05000278/2024002 IR 05000482/20240052024-08-14014 August 2024 Updated Inspection Plan for Wolf Creek Generating Station (Report 05000482/2024005) ML24225A1692024-08-12012 August 2024 10 CFR 50.46 Annual Report ML24222A6772024-08-0909 August 2024 Response to Request for Additional Information for Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition ML24214A3232024-08-0101 August 2024 Response to Request for Additional Information - Request for Alternative Schedule to Complete Decommissioning Beyond 60 Years of Permanent Cessation of Operations ML24208A0962024-07-25025 July 2024 57243-EN 57243 - Rssc Wire & Cable LLC, Dba Marmon - Part 21 Notification ML24206A1252024-07-24024 July 2024 Revision of Three Procedures and Two Forms That Implement the Radiological Emergency Response Plan (RERP) ML24191A0612024-07-0606 July 2024 Independent Spent Fuel Storage Installation (ISFSI) - Annual Radioactive Effluent Release Report ML24178A4142024-06-26026 June 2024 Revision of One Procedure and One Form That Implement the Radiological Emergency Response Plan (RERP) ML24178A3672024-06-26026 June 2024 Correction to 2023 Annual Radioactive Effluent Release Report – Report 47 ML24177A1512024-06-24024 June 2024 Post Accident Monitoring Instrumentation Report ML24166A1172024-06-20020 June 2024 Regulatory Audit Summary Regarding Proposed Alternative Schedule to Complete Decommissioning Beyond 60 Years RS-24-061, Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations2024-06-14014 June 2024 Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations IR 05000277/20243012024-06-13013 June 2024 Initial Operator Licensing Examination Report 05000277/2024301 and 05000278/2024301 RS-24-058, Regarding Subsequent License Renewal Environmental Review2024-06-0505 June 2024 Regarding Subsequent License Renewal Environmental Review ML24151A6482024-06-0303 June 2024 Changes in Reactor Decommissioning Branch Project Management Assignments for Some Decommissioning Facilities ML24150A2722024-05-29029 May 2024 Annual Radiological Environmental Operating Report 81, January 1, 2023 Through December 31, 2023 ML24150A0032024-05-28028 May 2024 Request for Exemptions from 10 CFR 50.82(a)(8)(i)(A) and 10 CFR 50.75(h)(1)(iv) and Proposed Amendment to the Decommissioning Trust Agreement ML24079A0762024-05-23023 May 2024 Issuance of Amendments to Adopt TSTF 264 RS-24-055, 2023 Corporate Regulatory Commitment Change Summary Report2024-05-17017 May 2024 2023 Corporate Regulatory Commitment Change Summary Report IR 05000277/20240012024-05-13013 May 2024 Integrated Inspection Report 05000277/2024001 and 05000278/2024001 ML24134A1792024-05-13013 May 2024 Supplemental Information in Support of Request for Alternative Schedule to Complete Decommissioning Beyond 60 Years of Permanent Cessation of Operations IR 05000277/20245012024-05-0808 May 2024 Emergency Preparedness Biennial Exercise Inspection Report 05000277/2024501 and 05000278/2024501 ML24121A1832024-04-30030 April 2024 Pre-Submittal Meeting Presentation Material Peach Bottom ECCS Compensated Level System Replacement Project RS-24-041, Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-04-30030 April 2024 Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24118A0032024-04-27027 April 2024 2023 Annual Radioactive Effluent Release Report - Report 47 ML24120A2762024-04-23023 April 2024 Independent Spent Fuel Storage Installation (ISFSI) Facility - Annual Radioactive Effluent Release Report 66 January 1, 2023 Through December 31, 2023 CNL-24-033, Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-04-17017 April 2024 Central Emergency Control Center Emergency Plan Implementing Procedure Revisions ML24107A2462024-04-15015 April 2024 Submittal of Changes to Technical Specifications Bases ML24103A2042024-04-12012 April 2024 Constellation Energy Generation, LLC, Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition ML24102A0472024-04-11011 April 2024 Operator Licensing Examination Approval 05000277/LER-2024-002, Uncoordinated DC Circuits Cause Unanalyzed Condition2024-04-0808 April 2024 Uncoordinated DC Circuits Cause Unanalyzed Condition RS-24-002, Constellation Energy Generation, LLC - Annual Property Insurance Status Report2024-04-0101 April 2024 Constellation Energy Generation, LLC - Annual Property Insurance Status Report RS-24-023, Report on Status of Decommissioning Funding.2024-03-22022 March 2024 Report on Status of Decommissioning Funding. IR 05000277/20244022024-03-12012 March 2024 Cybersecurity Inspection Report 05000277/2024402 and 05000278/2024402 (Cover Letter Only) ML24061A2642024-03-0101 March 2024 Revision of Two Procedures That Implement the Radiological Emergency Response Plan (RERP) for Wolf Creek Generating Station (WCGS) Commissioners ML24060A1192024-02-29029 February 2024 Notification of Conduct of a Fire Protection Team Inspection 2024-09-06
[Table view] Category:Licensee Response to Notice of Violation
MONTHYEARML23286A0012023-10-13013 October 2023 Reply to a Notice of Violation (NOV) - NOV 05000277, 05000278/2023010-01 ML23065A1582023-03-0606 March 2023 Reply to Notice of Violation (NCV 05000277, 05000278/2022004-01) ML0922205022009-08-0808 August 2009 Reply to a Notice of Violation: EA-09-029 ML0236103822002-12-19019 December 2002 Reply to a Notice of Violation (EA-02-142) Involving Emergency Classification 2023-03-06
[Table view] |
Text
10 CFR 2.201
CCN 23-67
October 13, 2023
U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001
Peach Bottom Atomic Power Station, Units 2 and 3 Subsequent Renewed Facility Operating License Nos. DPR-44 and DPR-56 NRC Docket Nos. 50-277 and 50-278
Subject:
Reply to a Notice of Violation (NOV) - NOV 05000277,05000278/2023010-01
Reference:
NRC Letter to Constellation Energy Generation, LLC, Peach Bottom Atomic Power Station, Units 2 and 3 - Biennial Problem Identification and Resolution Inspection Report 05000277/2023010 and 05000278/2023010 and Not ice of Violation, dated September 15, 2023 (ADAMS Accession No. ML2325 8A049) to this letter provides Constellation Energy Gener ations (CEG) reply to the Notice of Violation contained in Enclosure 2 to the referenced letter. The Notice of Violation was associated with failure to establish corrective action for erosion of structural backfill material in the pipe trench on the West side of the site.
This response includes a regulatory commitment, which is provid ed in Attachment 2. If you have any questions concerning this response, please contact the Peach Bottom Regulatory Assurance Manager, Wade Scott at (717) 456-3047.
Respectfully,
David A. Henry Site Vice President Peach Bottom Atomic Power Station
Attachments:
- 1. Reply to Notice of Violation (NOV) - NOV 05000277,05000278/2023010-01
- 2. Summary of Regulatory Commitments
cc: w/ Attachment Regional Administrator, Region I, USNRC USNRC Senior Resident Inspector, PBAPS Project Manager - PBAPS, USNRC W. DeHaas, Pennsylvania Bureau of Radiation Protection S. Seaman, State of Maryland Reply to a Notice of Violation (NOV) - NOV 05000277, 05000278/2 023010-01 Docket Nos. 50-277 and 50-278 Page 1 of 2
ATTACHMENT 1
Peach Bottom Atomic Power Station, Units 2 and 3
Docket Nos. 50-277 and 50-278
Reply to a Notice of Violation (NOV) - NOV 05000277, 05000278/2 023010-01
1.0 RESTATEMENT OF THE VIOLATION
10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in part, that measures shall be established to assure that conditions adverse to quali ty, such as deficiencies, defective material, and non-conformances are promptly identified and corr ected.
PI-AA-125, Corrective Action Program Procedure, Revision 7, s tep 4.5.2 states, in part, to create a corrective action for any planned actions necessary to restore a condition adverse to quality.
Contrary to the above, from at least May 10, 2021 to present, P each Bottom staff did not establish measures to correct the condition adverse to quality associated with the erosion of structural backfill material in the pipe trench.
This violation is associated with a Green Significance Determin ation Process finding.
2.0 REASON FOR THE VIOLATION
In August 2021, the NRC documented a finding and associated Non -Cited Violation (NCV) for the failure to correct a condition adverse to quality associate d with the erosion of structural backfill material in the pipe trench on the West side of the si te. The NCV was documented in NRC inspection report 05000277/2021012 and 05000278/2021012 (ML 21265A334). Although the site completed corrective actions to address the human perf ormance issues that resulted in the NCV, the NRC found that the site has not yet created correc tive actions to fully address the identified erosion due to ongoing troubleshooting of the condit ion. Confirmation of the suspected cause and the development of corrective actions is pr edicated on ongoing inspections of the drainage systems to gather data necessary to determine the cause of the erosion. The station acknowledges that insufficient resources had been dedicated to the completion of these actions and development of corrective actio ns for the settlement issue.
The station determined that the cause of the insufficient use o f resources was due to untimely prioritization due to misperception of risk.
Reply to a Notice of Violation (NOV) - NOV 05000277, 05000278/2 023010-01 Docket Nos. 50-277 and 50-278 Page 2 of 2
3.0 CORRECTIVE STEPS TAKEN AND RESULTS ACHIEVED
To date, the station has taken the following corrective steps:
- 1. Increased the frequency of inspection of pipe supports assoc iated with the affected piping to biannual. This action allows for increased monitorin g of the condition and will measure the effectiveness of future corrective actions.
- 2. Inspection of the storm drain system and identification of a reas of blockage. This information will be incorporated into the investigation revisio n, and ongoing efforts are in place to clear the drain.
- 3. Installation of a yard drain sump pump with setpoints that f acilitated inspection of the yard drainage piping and lowered the water levels in the area W est of the plant.
- 4. An inspection of yard drainage piping was recently performed which provides input to the investigation revision so that appropriate corrective actions c an be developed.
4.0 CORRECTIVE STEPS THAT WILL BE TAKEN
The station is revising CAPE 04424065 to incorporate the result s of the actions completed above, document the cause and establish the remaining correctiv e actions to address the erosion of structural backfill. A scope of work is being devel oped to fully mitigate the erosion in a timeframe commensurate with the safety significance of the is sue. A Project Manager has been assigned to ensure that the appropriate resources are prio ritized to resolve this issue.
5.0 DATE OF FULL COMPLIANCE
The station is implementing corrective actions through a revisi on to CAPE 04424065. This revision will be completed by December 1, 2023. At that time, corrective actions will be in place to assure that this condition will be promptly corrected, there by achieving full compliance.
Reply to a Notice of Violation (NOV) - NOV 05000277, 05000278/2 023010-01 Docket Nos. 50-277 and 50-278 Page 1 of 1
ATTACHMENT 2
SUMMARY
OF REGULATORY COMMITMENTS
The following table identifies commitments made in this documen t. (Any other actions discussed in the submittal represent intended or planned action s. They are described to the NRC for the NRCs information and are not regulatory commitment s.)
COMMITMENT COMMITTED DATE COMMITMENT TYPE OR OUTAGE ONE-TIME ACTION PROGRAMMATIC (Yes/No) (Yes/No)
Constellation December 1, 2023 Yes No Energy Generation, LLC, will develop and establish corrective actions to address the erosion of structural backfill in the pipe trench on the West side of the site.