IR 05000259/2009003: Difference between revisions

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{{Adams|number = ML092120168}}
{{Adams
| number = ML092120168
| issue date = 07/30/2009
| title = IR 05000259-09-003, 05000260-09-003 and 05000296-09-003, on 04/01/2009 - 06/30/2009, Browns Ferry Nuclear Plant, Units 1, 2 and 3, Maintenance Risk Assessment, Access Control to Radiologically Significant Areas, and Event Followup
| author name = Guthrie E F
| author affiliation = NRC/RGN-II/DRP/RPB6
| addressee name = Swafford P D
| addressee affiliation = Tennessee Valley Authority
| docket = 05000259, 05000260, 05000296
| license number = DPR-033, DPR-052, DPR-068
| contact person =
| case reference number = FOIA/PA-2010-0209
| document report number = IR-09-003
| document type = Inspection Report, Letter
| page count = 60
}}


{{IR-Nav| site = 05000259 | year = 2009 | report number = 003 }}
{{IR-Nav| site = 05000259 | year = 2009 | report number = 003 }}
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==Dear Mr. Swafford:==
==Dear Mr. Swafford:==
On June 30, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Browns Ferry Nuclear Plant, Units 1, 2, and 3. The enclosed inspection report documents the inspection results which were discussed, on July 6 and 17, 2009, with Mr. James Randich and other members of your staff. The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. In addition to the routine Reactor Oversight Process baseline inspections for all three units, the inspectors continued to conduct augmented inspections on Unit 1, as required, in accordance with NRC letters dated May 16, 2007, December 6, 2007, and May 21, 2008. These Unit 1 augmented inspections were conducted to compensate for the lack of valid data for the Mitigating Systems Performance Index (MSPI) Performance Indicators (PIs). The augmented inspections are only considered to be an interim substitute for the invalid Unit 1 MSPI PIs until such time as complete and accurate PI data is developed and declared valid. Based on the results of this inspection, one NRC-identified finding and three self-revealing findings of very low safety significance (Green) were identified. Three of these findings were determined to involve violations of NRC requirements. Additionally, a licensee-identified violation which was determined to be of very low safety significance is listed in this report. However, because of their very low safety significance and because they were entered into your corrective action program, the NRC is treating these findings as non-cited violations (NCV(s)) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Senior Resident Inspector at Browns Ferry Nuclear Plant.
On June 30, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Browns Ferry Nuclear Plant, Units 1, 2, and 3. The enclosed inspection report documents the inspection results which were discussed, on July 6 and 17, 2009, with Mr. James Randich and other members of your staff.
 
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
 
In addition to the routine Reactor Oversight Process baseline inspections for all three units, the inspectors continued to conduct augmented inspections on Unit 1, as required, in accordance with NRC letters dated May 16, 2007, December 6, 2007, and May 21, 2008. These Unit 1 augmented inspections were conducted to compensate for the lack of valid data for the Mitigating Systems Performance Index (MSPI) Performance Indicators (PIs). The augmented inspections are only considered to be an interim substitute for the invalid Unit 1 MSPI PIs until such time as complete and accurate PI data is developed and declared valid.
 
Based on the results of this inspection, one NRC-identified finding and three self-revealing findings of very low safety significance (Green) were identified. Three of these findings were determined to involve violations of NRC requirements. Additionally, a licensee-identified violation which was determined to be of very low safety significance is listed in this report. However, because of their very low safety significance and because they were entered into your corrective action program, the NRC is treating these findings as non-cited violations (NCV(s)) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Senior Resident Inspector at Browns Ferry Nuclear Plant.


TVA 2 In addition, if you disagree with the characterization of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at Browns Ferry Nuclear Plant. The information you provide will be considered in accordance with Inspection Manual Chapter 0305.
TVA 2 In addition, if you disagree with the characterization of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at Browns Ferry Nuclear Plant. The information you provide will be considered in accordance with Inspection Manual Chapter 0305.
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Sincerely,/RA/
Sincerely,/RA/
Eugene F. Guthrie, Chief Reactor Projects Branch 6 Division of Reactor Projects Docket Nos.: 50-259, 50-260, 50-296 License Nos.: DPR-33, DPR-52, DPR-68  
Eugene F. Guthrie, Chief Reactor Projects Branch 6 Division of Reactor Projects Docket Nos.: 50-259, 50-260, 50-296 License Nos.: DPR-33, DPR-52, DPR-68  


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===w/Attachment:===
===w/Attachment:===
Supplemental Information cc w/encl. (See page 3)
Supplemental Information  
TVA 2 In addition, if you disagree with the characterization of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at Browns Ferry Nuclear Plant. The information you provide will be considered in accordance with Inspection Manual Chapter 0305.
 
cc w/encl. (See page 3)  
 
_________________________ X SUNSI REVIEW COMPLETE OFFICE RII:DRP RII:DRP RII:DRP RII:DRP RII:DRS RII:DRS RII:DRS RII:DRS RII:DRP SIGNATURE PH TR by fax By email KK by emailRW by email BB for BB for BB for EG NAME PHiggins TRoss CStancil KKorth RWilliams HGepford RHamilton WLoo EGuthrie DATE 07/30/2009 07/30/2009 7/31/2009 07/30/2009 07/30/2009 7/31/2009 7/31/2009 7/31/2009 07/30/2009 E-MAIL COPY? YES/NO YES/NO YES/NO YES/NO YES/NO YES/NO YES/NO YES/NO YES/NO TVA 3 cc w/encl: Ashok S. Bhatnagar Senior Vice President Nuclear Generation Development and Construction 6A Lookout Place 1101 Market Street Chattanooga, TN 37402-2801 Preston Chief Nuclear Officer and Executive Vice President Tennessee Valley Authority 3R Lookout Place 1101 Market Street Chattanooga, TN 37402-2801 William R. Campbell Senior Vice President, Fleet Engineering Tennessee Valley Authority 6A Lookout Place 1101 Market Street Chattanooga, Tennessee 37402-2801
 
Tom Coutu Vice President Nuclear Support Tennessee Valley Authority 3R Lookout Place 1101 Market Street Chattanooga, TN 37402-2801 R. G. (Rusty) West Site Vice President Browns Ferry Nuclear Plant Tennessee Valley Authority Electronic Mail Distribution
 
Frederick Russell Godwin Manager, Licensing & Industry Affairs Browns Ferry Nuclear Plant Tennessee Valley Authority Electronic Mail Distribution James J. Randich Plant Manager Browns Ferry Nuclear Plant Tennessee Valley Authority Electronic Mail Distribution
 
General Counsel Tennessee Valley Authority 6A West Tower 400 West Summit Hill Drive Knoxville, TN 37902
 
Larry E. Nicholson General Manager Performance & Performance Improvement Tennessee Valley Authority Electronic Mail Distribution Michael A. Purcell Senior Licensing Manager Nuclear Power Group Tennessee Valley Authority Electronic Mail Distribution
 
Michael J. Lorek Interim Vice President Nuclear Engineering and Projects Tennessee Valley Authority Electronic Mail Distribution Fredrick C. Mashburn Acting Manager, Corporate Nuclear Licensing & Industry Affairs Tennessee Valley Authority Electronic Mail Distribution Mr. Robert J. Whalen Vice President, Nuclear Engineering Tennessee Valley Authority 3R Lookout Place 1101 Market Street Chattanooga, Tennessee 37402-2801
 
State Health Officer Alabama Dept. of Public Health RSA Tower - Administration Suite 1552 P.O. Box 303017 Montgomery, AL 36130-3017
 
Chairman Limestone County Commission 310 West Washington Street Athens, AL 35611 TVA 4 Letter to Preston from Eugene F. Guthrie dated July 30, 2009


In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response, if any, will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
SUBJECT: BROWNS FERRY NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT 05000259/2009003, 05000260/2009003 AND 05000296/2009003 Distribution w/encl:
E. Brown, NRR L. Raghavan, NRR C. Evans, RII L. Slack, RII T. Ross, SRI Browns Ferry OE Mail RIDSNRRDIRS PUBLIC Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION II


Sincerely,/RA/
Docket Nos.: 50-259, 50-260, 50-296  
Eugene F. Guthrie, Chief Reactor Projects Branch 6 Division of Reactor Projects Docket Nos.: 50-259, 50-260, 50-296 License Nos.: DPR-33, DPR-52, DPR-68


===Enclosure:===
License Nos.: DPR-33, DPR-52, DPR-68
Inspection Report 05000259/2009003, 05000260/2009003 and 05000296/2009003


===w/Attachment:===
Report No.: 05000259/2009003, 05000260/2009003 and 05000296/2009003 Licensee: Tennessee Valley Authority (TVA)
Supplemental Information cc w/encl. (See page 3)
Facility: Browns Ferry Nuclear Plant, Units 1, 2, and 3  


X PUBLICLY AVAILABLE G NON-PUBLICLY AVAILABLE G SENSITIVE X NON-SENSITIVE ADAMS: G Yes ACCESSION NUMBER:_________________________ X SUNSI REVIEW COMPLETE OFFICE RII:DRP RII:DRP RII:DRP RII:DRP RII:DRS RII:DRS RII:DRS RII:DRS RII:DRP SIGNATURE PH TR by fax By email KK by emailRW by email BB for BB for BB for EG NAME PHiggins TRoss CStancil KKorth RWilliams HGepford RHamilton WLoo EGuthrie DATE 07/30/2009 07/30/2009 7/31/2009 07/30/2009 07/30/2009 7/31/2009 7/31/2009 7/31/2009 07/30/2009 E-MAIL COPY? YES/NO YES/NO YES/NO YES/NO YES/NO YES/NO YES/NO YES/NO YES/NO OFFICIAL RECORD COPY DOCUMENT NAME: G:\DRPII\RPB6\BROWNS FERRY\REPORTS\2009\BF 09-03\BROWNSFERRYIR2009-003.DOC TVA 3 cc w/encl: Ashok S. Bhatnagar Senior Vice President Nuclear Generation Development and Construction 6A Lookout Place 1101 Market Street Chattanooga, TN 37402-2801 Preston Chief Nuclear Officer and Executive Vice President Tennessee Valley Authority 3R Lookout Place 1101 Market Street Chattanooga, TN 37402-2801 William R. Campbell Senior Vice President, Fleet Engineering Tennessee Valley Authority 6A Lookout Place 1101 Market Street Chattanooga, Tennessee 37402-2801 Tom Coutu Vice President Nuclear Support Tennessee Valley Authority 3R Lookout Place 1101 Market Street Chattanooga, TN 37402-2801 R. G. (Rusty) West Site Vice President Browns Ferry Nuclear Plant Tennessee Valley Authority Electronic Mail Distribution Frederick Russell Godwin Manager, Licensing & Industry Affairs Browns Ferry Nuclear Plant Tennessee Valley Authority Electronic Mail Distribution James J. Randich Plant Manager Browns Ferry Nuclear Plant Tennessee Valley Authority Electronic Mail Distribution General Counsel Tennessee Valley Authority 6A West Tower 400 West Summit Hill Drive Knoxville, TN 37902 Larry E. Nicholson General Manager Performance & Performance Improvement Tennessee Valley Authority Electronic Mail Distribution Michael A. Purcell Senior Licensing Manager Nuclear Power Group Tennessee Valley Authority Electronic Mail Distribution Michael J. Lorek Interim Vice President Nuclear Engineering and Projects Tennessee Valley Authority Electronic Mail Distribution Fredrick C. Mashburn Acting Manager, Corporate Nuclear Licensing & Industry Affairs Tennessee Valley Authority Electronic Mail Distribution Mr. Robert J. Whalen Vice President, Nuclear Engineering Tennessee Valley Authority 3R Lookout Place 1101 Market Street Chattanooga, Tennessee 37402-2801 State Health Officer Alabama Dept. of Public Health RSA Tower - Administration Suite 1552 P.O. Box 303017 Montgomery, AL 36130-3017 Chairman Limestone County Commission 310 West Washington Street Athens, AL 35611 TVA 4 Letter to Preston from Eugene F. Guthrie dated July 30, 2009
Location: Corner of Shaw and Nuclear Plant Roads Athens, AL 35611  


SUBJECT: BROWNS FERRY NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT 05000259/2009003, 05000260/2009003 AND 05000296/2009003 Distribution w/encl: E. Brown, NRR L. Raghavan, NRR C. Evans, RII L. Slack, RII T. Ross, SRI Browns Ferry OE Mail RIDSNRRDIRS PUBLIC Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION II Docket Nos.: 50-259, 50-260, 50-296 License Nos.: DPR-33, DPR-52, DPR-68 Report No.: 05000259/2009003, 05000260/2009003 and 05000296/2009003 Licensee: Tennessee Valley Authority (TVA) Facility: Browns Ferry Nuclear Plant, Units 1, 2, and 3 Location: Corner of Shaw and Nuclear Plant Roads Athens, AL 35611 Dates: April 1, 2009 through June 30, 2009 Inspectors: T. Ross, Senior Resident Inspector C. Stancil, Resident Inspector K. Korth, Resident Inspector R. Williams, Reactor Inspector (1R08) H. Gepford, Senior Health Physicist (2OS1, 2PS1, 4OA1, 4OA7) R. Hamilton, Senior Health Physicist (2OS2)
Dates: April 1, 2009 through June 30, 2009 Inspectors: T. Ross, Senior Resident Inspector C. Stancil, Resident Inspector K. Korth, Resident Inspector R. Williams, Reactor Inspector (1R08) H. Gepford, Senior Health Physicist (2OS1, 2PS1, 4OA1, 4OA7) R. Hamilton, Senior Health Physicist (2OS2)
W. Loo, Senior Health Physicist (2PS2) Approved by: Eugene F. Guthrie, Chief Reactor Projects Branch 6 Division of Reactor Projects  
W. Loo, Senior Health Physicist (2PS2)
Approved by: Eugene F. Guthrie, Chief Reactor Projects Branch 6 Division of Reactor Projects  


Enclosure  
Enclosure  


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
IR 05000259/2009003, 05000260/2009003 and 05000296/2009003; 04/01/2009 - 06/30/2009; Browns Ferry Nuclear Plant, Units 1, 2 and 3; Maintenance Risk Assessment, Access Control to Radiologically Significant Areas, and Event Followup.
IR 05000259/2009003, 05000260/2009003 and 05000296/2009003; 04/01/2009 - 06/30/2009; Browns Ferry Nuclear Plant, Units 1, 2 and 3;  


The report covered a three month period of inspection by resident inspectors and reactor inspectors from the region. Three non-cited violations (NCV) and one Finding (FIN) were identified. The significance of most findings is identified by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process" Revision 4, dated December 2006.
Maintenance Risk Assessment, Access Control to Radiologically Significant Areas, and Event Followup.
 
The report covered a three month period of inspection by resident inspectors and reactor inspectors from the region
. Three non-cited violations (NCV) and one Finding (FIN) were identified. The significance of most findings is identified by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process" Revision 4, dated December 2006.


===A. NRC Identified and Self-Revealing Findings===
===A. NRC Identified and Self-Revealing Findings===
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===Cornerstone: Initiating Events===
===Cornerstone: Initiating Events===
: '''Green.'''
: '''Green.'''
A Green self-revealing finding was identified for a failure to implement corrective actions in a timely manner to address excessive isophase bus cooling (IBC) system condensation that resulted in a main generator trip and Unit 1 reactor scram caused by water accumulation in the IBC ductwork, which created an electrical ground fault on the main generator isophase busses. An additional drain line was subsequently installed, and operating procedures were revised, to ensure any excessive condensation buildup would be removed from the IBC system during winter operation. This event was entered into the licensee's corrective action program as PER 163815. This finding was determined to be greater than minor because it was associated with the Initiating Event Cornerstone attribute of Equipment Performance, and adversely affected the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during at-power operations. The finding was evaluated using Phase 1 of the At-Power Significance Determination Process, and was determined to be of very low safety significance (Green) because it did not contribute to both the likelihood of a reactor trip and the likelihood that mitigating equipment or functions were not available. The cause of this finding was directly related to the cross-cutting aspect of appropriate and timely corrective actions in the area of Problem Identification and Resolution because the license had identified an abnormal equipment condition related to excessive IBC system condensation for which specified corrective actions were not carried out (P.1.d).  (Section 4OA3.2)  
A Green self-revealing finding was identified for a failure to implement corrective actions in a timely manner to address excessive isophase bus cooling (IBC) system condensation that resulted in a main generator trip and Unit 1 reactor scram caused by water accumulation in the IBC ductwork, which created an electrical ground fault on the main generator isophase busses. An additional drain line was subsequently installed, and operating procedures were revised, to ensure any excessive condensation buildup would be removed from the IBC system during winter operation. This event was entered into the licensee's corrective action program as PER 163815.
 
This finding was determined to be greater than minor because it was associated with the Initiating Event Cornerstone attribute of Equipment Performance, and adversely affected the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during at-power operations. The finding was evaluated using Phase 1 of the At-Power Significance Determination Process, and was determined to be of very low safety significance (Green) because it did not contribute to both the likelihood of a reactor trip and the likelihood that mitigating equipment or functions were not available. The cause of this finding was directly related to the cross-cutting aspect of appropriate and timely corrective actions in the area of Problem Identification and Resolution because the license had identified an abnormal equipment condition related to excessive IBC system condensation for which specified corrective actions were not carried out (P.1.d).  (Section 4OA3.2)


===Cornerstone: Mitigating Systems===
===Cornerstone: Mitigating Systems===
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===Cornerstone: Occupational Radiation Safety===
===Cornerstone: Occupational Radiation Safety===
* Green  A Green self-revealing non-cited violation of Technical Specifications 5.4.1, Procedures, was identified for a radiation worker who failed to follow the requirements of Radiation Work Permit 09270081 as required by procedure RCI-9.1, Radiation Work Permits, Rev. 57. The licensee has entered this issue into the corrective action program as problem evaluation report 171375. This finding is greater than minor because it is associated with the Occupational Radiation Safety Cornerstone attribute of Program and Process (Exposure Control) and adversely affected the cornerstone objective of ensuring adequate protection of worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation. The finding was evaluated using the Occupational Radiation Safety Significance Determination Process and determined to be of very low safety significance (Green) because it was not related to As Low As Reasonably Achievable (ALARA) planning, nor did it involve an overexposure or substantial potential for overexposure, and the ability to assess dose was not compromised. The cause of this finding was directly related to the cross-cutting aspect of work practices in the area of Human Performance, because the radiation worker failed to use self-checking prior to passing through the swing gate into the posted high radiation area (H.4.a).  (Section 2OS1)
* Green  A Green self-revealing non-cited violation of Technical Specifications 5.4.1, Procedures, was identified for a radiation worker who failed to follow the requirements of Radiation Work Permit 09270081 as required by procedure RCI-9.1, Radiation Work Permits, Rev. 57. The licensee has entered this issue into the corrective action program as problem evaluation report 171375. This finding is greater than minor because it is associated with the Occupational Radiation Safety Cornerstone attribute of Program and Process (Exposure Control) and adversely affected the cornerstone objective of ensuring adequate protection of worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation. The finding was evaluated using the Occupational Radiation Safety Significance Determination Process and determined to be of very low safety significance (Green) because it was not related to As Low As Reasonably Achievable (ALARA) planning, nor did it involve an overexposure or substantial potential for overexposure, and the ability to assess dose was not compromised. The cause of this finding was directly related to the cross-cutting aspect of work practices in the area of Human Performance, because the radiation worker failed to use self-checking prior to passing through the swing gate into the posted high radiation area (H.4.a).  (Section 2OS1)  


===B. Licensee Identified Violations===
===B. Licensee Identified Violations===
One violation of very low safety significance, which was identified by the licensee, has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. This violation and the corrective action program tracking number are listed in Section 4OA7 of this report.
One violation of very low safety significance, which was identified by the licensee, has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. This violation and the corrective action program tracking number are listed in Section 4OA7 of this report.


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===Summary of Plant Status===
===Summary of Plant Status===
Unit 1 operated at full rated thermal power (RTP) the entire report period except for three planned downpowers. On May 2, 2009, a planned downpower to approximately 90 percent RTP was conducted to perform a control rod adjustment. The unit was returned to full RTP the same day. On June 6, 2009, a planned downpower to approximately 70 percent RTP was conducted to execute a control rod sequence exchange. The unit was returned to full RTP the same day. On June 12, 2009, a planned downpower to approximately 75 percent RTP was conducted to repair Main Turbine Generator #3 Control Valve. The unit was returned to full RTP the same day. Unit 2 began this report period at full RTP. On April 11, 2009, a planned downpower to 80 percent RTP was conducted to execute a control rod adjustment. The unit returned to full RTP on the same day. On April 25, 2009, the unit was shutdown for the Unit 2 Cycle 15 (U2C15) refueling outage. The unit was restarted June 8, 2009, but had to shutdown from approximately 15 percent RTP due to a sudden increase in unidentified reactor coolant system (RCS) leakage in excess of the Technical Specification limit of 2 gallons per minute in the previous 24 hours. Following repairs, the reactor was restarted on June 15, 2009. The unit was shutdown again from approximately 14 percent RTP on June 16, 2009 due to failure of the same MSRV to properly lift and reseat during testing. After the MSRV was replaced, Unit 2 was restarted on June 20, 2009. The unit achieved full RTP power on June 27, 2009 and remained at full RTP for the remainder of the report period.
 
Unit 1 operated at full rated thermal power (RTP) the entire report period except for three planned downpowers. On May 2, 2009, a planned downpower to approximately 90 percent RTP was conducted to perform a control rod adjustment. The unit was returned to full RTP the same day. On June 6, 2009, a planned downpower to approximately 70 percent RTP was conducted to execute a control rod sequence exchange. The unit was returned to full RTP the same day. On June 12, 2009, a planned downpower to approximately 75 percent RTP was conducted to repair Main Turbine Generator #3 Control Valve. The unit was returned to full RTP the same day.
 
Unit 2 began this report period at full RTP.
 
On April 11, 2009, a planned downpower to 80 percent RTP was conducted to execute a control rod adjustment. The unit returned to full RTP on the same day. On April 25, 2009, the unit was shutdown for the Unit 2 Cycle 15 (U2C15) refueling outage. The unit was restarted June 8, 2009, but had to shutdown from approximately 15 percent RTP due to a sudden increase in unidentified reactor coolant system (RCS) leakage in excess of the Technical Specification limit of 2 gallons per minute in the previous 24 hours. Following repairs, the reactor was restarted on June 15, 2009. The unit was shutdown again from approximately 14 percent RTP on June 16, 2009 due to failure of the same MSRV to properly lift and reseat during testing. After the MSRV was replaced, Unit 2 was restarted on June 20, 2009. The unit achieved full RTP power on June 27, 2009 and remained at full RTP for the remainder of the report period.


Unit 3 operated at full RTP the entire report period except for eight planned downpowers. Four of the power reductions were conducted to between 90 and 95 percent RTP to repair reactor feedwater heater or moisture separator normal level control valves. These downpowers were conducted on April 3, May 22, May 29, and June 23, 2009, and in each case, power was restored to full RTP on the same day. On April 4, 2009, a downpower was conducted to 75 percent RTP for a control rod adjustment. On April 15, 2009, a downpower to approximately 58 percent RTP was conducted to replace two power cells in the 3B Variable Frequency Drive.
Unit 3 operated at full RTP the entire report period except for eight planned downpowers. Four of the power reductions were conducted to between 90 and 95 percent RTP to repair reactor feedwater heater or moisture separator normal level control valves. These downpowers were conducted on April 3, May 22, May 29, and June 23, 2009, and in each case, power was restored to full RTP on the same day. On April 4, 2009, a downpower was conducted to 75 percent RTP for a control rod adjustment. On April 15, 2009, a downpower to approximately 58 percent RTP was conducted to replace two power cells in the 3B Variable Frequency Drive.
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==REACTOR SAFETY==
==REACTOR SAFETY==
Cornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity 1R01 Adverse Weather Protection
Cornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity  
 
{{a|1R01}}
==1R01 Adverse Weather Protection==


===.1 Readiness for Seasonal Extreme Weather Conditions===
===.1 Readiness for Seasonal Extreme Weather Conditions===
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors conducted three equipment partial alignment walkdowns to evaluate the operability of selected redundant trains or backup systems, listed below, with the other train or system inoperable or out of service. The inspectors reviewed the functional systems descriptions, Updated Final Safety Analysis Report (UFSAR), system operating procedures, and Technical Specifications (TS) to determine correct system lineups for the current plant conditions. The inspectors performed walkdowns of the systems to verify that critical components were properly aligned and to identify any discrepancies which could affect operability of the redundant train or backup system.
The inspectors conducted three equipment partial alignment walkdowns to evaluate the operability of selected redundant trains or backup systems, listed below, with the other train or system inoperable or out of service. The inspectors reviewed the functional systems descriptions, Updated Final Safety Analysis Report (UFSAR), system operating procedures, and Technical Specifications (TS) to determine correct system lineups for the current plant conditions. The inspectors performed walkdowns of the systems to verify that critical components were properly aligned and to identify any discrepancies which could affect operability of the redundant train or backup system.
7 Enclosure
* Unit 2 Core Spray (CS) System, Division II
* Unit 2 Core Spray (CS) System, Division II
* Unit 3 High Pressure Coolant Injection (HPCI) System
* Unit 3 High Pressure Coolant Injection (HPCI) System
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The inspectors' review of NDE activities specifically covered examination procedures, NDE reports, equipment and consumables certification records, personnel qualification records, and calibration reports (as applicable) for the following examinations:
The inspectors' review of NDE activities specifically covered examination procedures, NDE reports, equipment and consumables certification records, personnel qualification records, and calibration reports (as applicable) for the following examinations:
* Liquid penetrant (PT) and visual exam (VT-3) of component 2-47B408S0043 and its integrated attachment, ASME Class 1 Category B-K, welded attachment
* Liquid penetrant (PT) and visual exam (VT-3) of component 2-47B408S0043 and its integrated attachment, ASME Class 1 Category B-K, welded attachment
* Phased array ultrasonic testing (UT) examination of weld GFW-2-32, ASME Class 1 Category B-J, Tee to pipe weld The inspectors reviewed the following examination from the previous outage with a relevant indication that was analytically evaluated and accepted for continued service to verify that the acceptance was in accordance with ASME Code:
* Phased array ultrasonic testing (UT) examination of weld GFW-2-32, ASME Class 1 Category B-J, Tee to pipe weld The inspectors reviewed the following examination from the previous outage with a relevant indication that was analytically evaluated and accepted for continued service to verify that the acceptance was in accordance with ASME Code:
* NOI #U2C14-049 - N9 nozzle to vessel weld The inspectors' review of welding activities specifically covered the welding activity listed below in order to evaluate compliance with procedures and the ASME Code. The inspector reviewed the work order, repair and replacement plan, weld data sheets, welding procedures, procedure qualification records, welder qualification records, and NDE reports.
* NOI #U2C14-049 - N9 nozzle to vessel weld The inspectors' review of welding activities specifically covered the welding activity listed below in order to evaluate compliance with procedures and the ASME Code. The inspector reviewed the work order, repair and replacement plan, weld data sheets, welding procedures, procedure qualification records, welder qualification records, and NDE reports.
* Welding package for work order #09-711929-000 - Welded replacement of valve BFR-1-SHV-067-0655
* Welding package for work order #09-711929-000 - Welded replacement of valve BFR-1-SHV-067-0655


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The inspectors reviewed the following NDE activities associated with the inspection of reactor vessel internal components per the BWRVIP:
The inspectors reviewed the following NDE activities associated with the inspection of reactor vessel internal components per the BWRVIP:
* EVT-1 of Jet Pump restrainer assemblies including the set screws and wedge assemblies
* EVT-1 of Jet Pump restrainer assemblies including the set screws and wedge assemblies
* VT-3 of feed water sparger pins 9 Enclosure The inspectors also reviewed activities related to the planned repair and modification of select jet pump restrainer assemblies. For some assemblies, larger-than-allowable gaps between the jet pumps and set screws were seen during the visual examinations. The inspectors verified that planned repairs were being completed in accordance with BWRVIP requirements.
* VT-3 of feed water sparger pins  
 
9 Enclosure The inspectors also reviewed activities related to the planned repair and modification of select jet pump restrainer assemblies. For some assemblies, larger-than-allowable gaps between the jet pumps and set screws were seen during the visual examinations. The inspectors verified that planned repairs were being completed in accordance with BWRVIP requirements.


====b. Findings====
====b. Findings====
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=====Introduction:=====
=====Introduction:=====
A self-revealing non-cited violation (NCV) of 10 CFR Part 50.65 (a)(4), "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants," was identified for failure to adequately assess and manage shutdown risk associated with outage maintenance activities. Specifically, on May 2, 2009, the licensee performed a scheduled activity to install the 2A Reactor Recirculation suction line nozzle plug in the reactor vessel. This plug isolated the common shutdown cooling (SDC) suction path while SDC was assumed to be available in the existing outage risk assessment and had been designated as protected equipment .
A self-revealing non-cited violation (NCV) of 10 CFR Part 50.65 (a)(4), "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants," was identified for failure to adequately assess and manage shutdown risk associated with outage maintenance activities. Specifically, on May 2, 2009, the licensee performed a scheduled activity to install the 2A Reactor Recirculation suction line nozzle plug in the reactor vessel. This plug isolated the common shutdown cooling (SDC) suction path while SDC was assumed to be available in the existing outage risk assessment and had been designated as protected equipment .


=====Description:=====
=====Description:=====
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=====Analysis:=====
=====Analysis:=====
The inspectors determined that the risk management actions put in place pursuant to 10 CFR 50.65(a)(4) for in progress outage maintenance activities were not effectively managed to prevent disabling the protected SDC system and constituted a performance deficiency. This finding affected the Mitigating Systems cornerstone and was determined to be greater than minor according to Inspection Manual Chapter (IMC)0612, Appendix B, Issue Screening, because the licensee failed to effectively manage the prescribed significant compensatory measures (i.e. protection of Loop I RHR). The significance of this finding was evaluated using IMC 0609, Appendix K, Maintenance Risk Assessment and Risk Management Significance Determination Process, which stated that if the finding involved maintenance activities during shutdown conditions, then the appropriate checklist reflecting the plant shutdown mode from IMC 0609, Appendix G, Attachment 1, should be checked to determine risk significance. According to IMC 0609, Appendix G, "Shutdown Operations Significance Determination Process," Table 1, "Losses of Control," and Checklist 7 of Attachment 1, "BWR Refueling Operation with RCS Level > 23'" , the inspectors determined that this finding was of very low safety significance (Green) because the event did not result a loss of control per Table 1 of MC0609, Appendix G, or an actual loss of decay heat removal and the SDC alignment was restored well within the time to boil. As such, Appendix G did not require the significance of the finding to be quantified by a Phase 2 or 3 analysis. During the event, ADHR was in service removing reactor decay heat, and there was adequate time to restore SDC to service (i.e., remove the plug) before boiling of the RCS would occur if ADHR were lost (i.e., time to boil about 24 hours). The RHR SDC function was restored in a relatively short period of time (approximately 6 hours). The cause of this finding was directly related to the cross cutting aspect of work activity coordination in the area of Human Performance, because the licensee failed to adequately evaluate the impact of the work and to communicate, coordinate, and cooperate with each other during activities in which interdepartmental coordination is necessary to assure plant performance. Specifically, the OCC authorized installation of the recirculation line plug even though the plant was relying on SDC availability as defense in depth for their shutdown risk assessment (H.3.b).  
The inspectors determined that the risk management actions put in place pursuant to 10 CFR 50.65(a)(4) for in progress outage maintenance activities were not effectively managed to prevent disabling the protected SDC system and constituted a performance deficiency. This finding affected the Mitigating Systems cornerstone and was determined to be greater than minor according to Inspection Manual Chapter (IMC)0612, Appendix B, Issue Screening, because the licensee failed to effectively manage the prescribed significant compensatory measures (i.e. protection of Loop I RHR). The significance of this finding was evaluated using IMC 0609, Appendix K, Maintenance Risk Assessment and Risk Management Significance Determination Process, which stated that if the finding involved maintenance activities during shutdown conditions, then the appropriate checklist reflecting the plant shutdown mode from IMC 0609, Appendix G, Attachment 1, should be checked to determine risk significance. According to IMC 0609, Appendix G, "Shutdown Operations Significance Determination Process," Table 1, "Losses of Control," and Checklist 7 of Attachment 1, "BWR Refueling Operation with RCS Level > 23'" , the inspectors determined that this finding was of very low safety significance (Green) because the event did not result a loss of control per Table 1 of MC0609, Appendix G, or an actual loss of decay heat removal and the SDC alignment was restored well within the time to boil. As such, Appendix G did not require the significance of the finding to be quantified by a Phase 2 or 3 analysis. During the event, ADHR was in service removing reactor decay heat, and there was adequate time to restore SDC to service (i.e., remove the plug) before boiling of the RCS would occur if ADHR were lost (i.e., time to boil about 24 hours). The RHR SDC function was restored in a relatively short period of time (approximately 6 hours). The cause of this finding was directly related to the cross cutting aspect of work activity coordination in the area of Human Performance, because the licensee failed to adequately evaluate the impact of the work and to communicate, coordinate, and cooperate with each other during activities in which interdepartmental coordination is necessary to assure plant performance. Specifically, the OCC authorized installation of the recirculation line plug even though the plant was relying on SDC availability as defense in depth for their shutdown risk assessment (H.3.b).


=====Enforcement:=====
=====Enforcement:=====
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=====Description:=====
=====Description:=====
At 1550, on May 1, 2009, with Unit 1 at 100 percent power, the licensee removed the A EDG from service for planned maintenance while the A3 EECW pump and the RHR crosstie were already OOS. At 1611, a Tornado Warning was issued by the National Weather Service. However, the licensee failed to re-evaluate their risk assessment prior to, or during the onset of, severe weather conditions to consider the potential impact of severe weather on plant risk. The Tornado Warning expired at 1715. Then on May 2, 2009, the A EDG was declared inoperable for surveillance testing at 1503. At 1510, a Tornado Watch was issued by the National Weather Service. The licensee aborted the diesel surveillance and restored it to service, but severe weather conditions were not considered in the risk assessment either before or afterwards. Section 3.2.A, of Standards Programs and Processes (SPP) 7.1, On-Line Work Management, required that a risk assessment of scheduled on-line maintenance be performed prior to implementation, and emergent work was to be evaluated against the assessed scope. According to section 3.2.B.1.n of SPP 7.1, this risk assessment was required to include external event considerations involving the potential impacts of weather or other external conditions relative to the proposed maintenance evolution if these external impacts (e.g., weather, external flooding, grid reliability, and other external impacts) were imminent or have a high probability of occurring during the planned out of service duration. Furthermore, section 3.2.2 of SPP 7.1, required that the assessment of risk for scheduled activities be re-performed if there were significant changes in external conditions (e.g., weather or offsite power availability). The licensee's failure to consider severe weather conditions as part of their on-line risk assessments on May 1 and 2, 2009, were contrary to the provisions of SPP-7.1.
At 1550, on May 1, 2009, with Unit 1 at 100 percent power, the licensee removed the A EDG from service for planned maintenance while the A3 EECW pump and the RHR crosstie were already OOS. At 1611, a Tornado Warning was issued by the National Weather Service. However, the licensee failed to re-evaluate their risk assessment prior to, or during the onset of, severe weather conditions to consider the potential impact of severe weather on plant risk. The Tornado Warning expired at 1715. Then on May 2, 2009, the A EDG was declared inoperable for surveillance testing at 1503. At 1510, a Tornado Watch was issued by the National Weather Service. The licensee aborted the diesel surveillance and restored it to service, but severe weather conditions were not considered in the risk assessment either before or afterwards.
 
Section 3.2.A, of Standards Programs and Processes (SPP) 7.1, On-Line Work Management, required that a risk assessment of scheduled on-line maintenance be performed prior to implementation, and emergent work was to be evaluated against the assessed scope. According to section 3.2.B.1.n of SPP 7.1, this risk assessment was required to include external event considerations involving the potential impacts of weather or other external conditions relative to the proposed maintenance evolution if these external impacts (e.g., weather, external flooding, grid reliability, and other external impacts) were imminent or have a high probability of occurring during the planned out of service duration. Furthermore, section 3.2.2 of SPP 7.1, required that the assessment of risk for scheduled activities be re-performed if there were significant changes in external conditions (e.g., weather or offsite power availability). The licensee's failure to consider severe weather conditions as part of their on-line risk assessments on May 1 and 2, 2009, were contrary to the provisions of SPP-7.1.


The sub-tier instructions used by the licensee for assessing on-line risk at Browns Ferry included BP-336, Risk Determination and Risk Management, and 0-TI-367, BFN Equipment to Plant Risk Matrix. These Browns Ferry site specific guidelines did not include consideration of severe weather impact on on-line risk.
The sub-tier instructions used by the licensee for assessing on-line risk at Browns Ferry included BP-336, Risk Determination and Risk Management, and 0-TI-367, BFN Equipment to Plant Risk Matrix. These Browns Ferry site specific guidelines did not include consideration of severe weather impact on on-line risk.
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The failure of the licensee to consider the impact of severe weather on plant risk was a performance deficiency which could have led to underestimating the risk of plant maintenance activities and/or failure to take actions to minimize that risk. This finding was determined to be greater than minor according to IMC 0612, Appendix B, Issue Screening, because the licensee's risk assessment failed to consider unusual external conditions that were present or imminent (e.g., severe weather, offsite power instability). The significance of this finding was determined to be of very low safety significance (Green) according to IMC 0609, Appendix K, Maintenance Risk Assessment 14 Enclosure and Risk Management Significance Determination Process, based on an initiating events frequency of <1.0E-7, and a very low risk deficit due to the number of redundant emergency diesels and the short duration of the severe weather. This issue was entered into the licensee's corrective action program as PER 171402.
The failure of the licensee to consider the impact of severe weather on plant risk was a performance deficiency which could have led to underestimating the risk of plant maintenance activities and/or failure to take actions to minimize that risk. This finding was determined to be greater than minor according to IMC 0612, Appendix B, Issue Screening, because the licensee's risk assessment failed to consider unusual external conditions that were present or imminent (e.g., severe weather, offsite power instability). The significance of this finding was determined to be of very low safety significance (Green) according to IMC 0609, Appendix K, Maintenance Risk Assessment 14 Enclosure and Risk Management Significance Determination Process, based on an initiating events frequency of <1.0E-7, and a very low risk deficit due to the number of redundant emergency diesels and the short duration of the severe weather. This issue was entered into the licensee's corrective action program as PER 171402.


The cause of this finding was directly related to the crosscutting aspect of complete and accurate procedures in the area of Human Performance because the licensee's site specific guidelines for assessing on-line risk did not require severe weather to be considered when determining plant risk nor did they require personnel to determine if severe weather is imminent prior to removing an emergency diesel generator from service (H.2.c).  
The cause of this finding was directly related to the crosscutting aspect of complete and accurate procedures in the area of Human Performance because the licensee's site specific guidelines for assessing on-line risk did not require severe weather to be considered when determining plant risk nor did they require personnel to determine if severe weather is imminent prior to removing an emergency diesel generator from service (H.2.c).


=====Enforcement:=====
=====Enforcement:=====
10 CFR 50.65 (a)(4), required in part, that before performing maintenance activities (including but not limited to surveillance, post-maintenance testing, and corrective and preventive maintenance), the licensee shall assess and manage the increase in risk that may result from the proposed maintenance activities. Contrary to this, on May 1 and 2, 2009, plant personnel failed to assess and manage risk for maintenance activities during unusual external conditions (i.e., severe weather).
10 CFR 50.65 (a)(4), required in part, that before performing maintenance activities (including but not limited to surveillance, post-maintenance testing, and corrective and preventive maintenance), the licensee shall assess and manage the increase in risk that may result from the proposed maintenance activities. Contrary to this, on May 1 and 2, 2009, plant personnel failed to assess and manage risk for maintenance activities during unusual external conditions (i.e., severe weather).


Because this finding was determined to be of very safety risk significance (Green) and has been entered into the licensee's CAP as PER 171402, this violation is being treated as an NCV, consistent with Section VI.A of the Enforcement Policy: NCV 05000259/2009003-02, "Failure to Perform an Adequate Risk Assessment during Severe Weather Conditions." 1R15 Operability Evaluations
Because this finding was determined to be of very safety risk significance (Green) and has been entered into the licensee's CAP as PER 171402, this violation is being treated as an NCV, consistent with Section VI.A of the Enforcement Policy: NCV 05000259/2009003-02, "Failure to Perform an Adequate Risk Assessment during Severe Weather Conditions."
 
{{a|1R15}}
==1R15 Operability Evaluations==


====a. Inspection Scope====
====a. Inspection Scope====
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the Design Change Notice (DCN) and completed work packages (WO 08-724013-018 and 08-724013-21) for DCN 69528, Replace ASCO Solenoid Valves with Similar AVCO Valves, including related documents and procedures. The inspectors reviewed licensee procedures 0-TI-405, Plant Modifications and Design Change Control, and SPP-9.3, Plant Modifications and Engineering Change Control, and observed part of the licensee=s activities to implement this design change made while the unit was online. The inspectors reviewed the associated 10 CFR 50.59 screening against the system design bases documentation to verify that the modifications had not affected system operability/availability. The inspectors reviewed selected ongoing and completed work activities to verify that installation was consistent with the design control documents.
The inspectors reviewed the Design Change Notice (DCN) and completed work packages (WO 08-724013-018 and 08-724013-21) for DCN 69528, Replace ASCO Solenoid Valves with Similar AVCO Valves, including related documents and procedures. The inspectors reviewed licensee procedures 0-TI-405, Plant Modifications and Design Change Control, and SPP-9.3, Plant Modifications and Engineering Change Control, and observed part of the licensee
=s activities to implement this design change made while the unit was online. The inspectors reviewed the associated 10 CFR 50.59 screening against the system design bases documentation to verify that the modifications had not affected system operability/availability. The inspectors reviewed selected ongoing and completed work activities to verify that installation was consistent with the design control documents.


====b. Findings====
====b. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
During April 25 to June 26, 2009, the inspectors examined critical outage activities to verify that they were conducted in accordance with TS, applicable procedures, and the licensee's outage risk assessment and management plans through the end of the reporting period. Some of the more significant inspection activities conducted by the inspectors were as follows: Outage Risk Assessment   Prior to the Unit 2 Cycle 15 (U2C15) refueling outage that began on April 25, the inspectors attended outage risk assessment team meetings and reviewed the Outage Risk Assessment Report to verify that the licensee had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing an outage plan that assured defense-in-depth of safety functions were maintained. The inspectors also reviewed the daily U2C15 Refueling Outage Reports, including the ORAM Safety Function Status, and regularly attended the twice a day outage status meetings. These reviews were compared to the requirements in licensee procedure SPP-7.2, Outage Management, SPP-7.3, Work Activity Risk Management Process, and TS. These reviews were also done to verify that for identified increased risk significant conditions, due to equipment availability and/or system configurations, contingency measures were identified and incorporated into the overall outage and contingency response plan. Furthermore, the inspectors frequently discussed risk conditions and designated protected equipment with Operations and outage management personnel to assess licensee awareness of actual risk conditions and mitigation strategies. Shutdown and Cooldown Process  The inspectors witnessed the shutdown and cooldown of Unit 2 in accordance with licensee procedures SPP-12.1, Conduct of Operations; 2-GOI-100-12A, Unit Shutdown from Power Operations to Cold Shutdown and Reduction in Power During Power Operations; and 2-SR-3.4.9.1(1), Reactor Heatup or Cooldown Rate Monitoring. Decay Heat Removal  The inspectors reviewed licensee procedures 2-OI-74, Residual Heat Removal System (RHR); 2-OI-78, Fuel Pool Cooling and Cleanup System; and Abnormal Operating Instruction 0-AOI-72-1, Alternate Decay Heat Removal System Failures; and conducted a main control room panel and in-plant walkdowns of system and components to verify correct system alignment. In addition, the inspectors reviewed controls implemented to ensure that outage work was not impacting the ability of operators to operate spent fuel pool cooling, RHR shutdown cooling, and/or ADHR system. Furthermore, the inspectors conducted several walkdowns of the ADHR system during operation with the fuel pool gates removed.
During April 25 to June 26, 2009, the inspectors examined critical outage activities to verify that they were conducted in accordance with TS, applicable procedures, and the licensee's outage risk assessment and management plans through the end of the reporting period. Some of the more significant inspection activities conducted by the inspectors were as follows:
Outage Risk Assessment Prior to the Unit 2 Cycle 15 (U2C15) refueling outage that began on April 25, the inspectors attended outage risk assessment team meetings and reviewed the Outage Risk Assessment Report to verify that the licensee had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing an outage plan that assured defense-in-depth of safety functions were maintained. The inspectors also reviewed the daily U2C15 Refueling Outage Reports, including the ORAM Safety Function Status, and regularly attended the twice a day outage status meetings. These reviews were compared to the requirements in licensee procedure SPP-7.2, Outage Management, SPP-7.3, Work Activity Risk Management Process, and TS. These reviews were also done to verify that for identified increased risk significant conditions, due to equipment availability and/or system configurations, contingency measures were identified and incorporated into the overall outage and contingency response plan. Furthermore, the inspectors frequently discussed risk conditions and designated protected equipment with Operations and outage management personnel to assess licensee awareness of actual risk conditions and mitigation strategies.


Critical Outage Activities The inspectors examined outage activities to verify that they were conducted in accordance with TS, licensee procedures, and the licensee's outage risk control plan. Some of the more significant inspection activities accomplished by the inspectors were as follows:
Shutdown and Cooldown Process The inspectors witnessed the shutdown and cooldown of Unit 2 in accordance with licensee procedures SPP-12.1, Conduct of Operations; 2-GOI-100-12A, Unit Shutdown from Power Operations to Cold Shutdown and Reduction in Power During Power Operations; and 2-SR-3.4.9.1(1), Reactor Heatup or Cooldown Rate Monitoring.
 
Decay Heat Removal The inspectors reviewed licensee procedures 2-OI-74, Residual Heat Removal System (RHR); 2-OI-78, Fuel Pool Cooling and Cleanup System; and Abnormal Operating Instruction 0-AOI-72-1, Alternate Decay Heat Removal System Failures; and conducted a main control room panel and in-plant walkdowns of system and components to verify correct system alignment. In addition, the inspectors reviewed controls implemented to ensure that outage work was not impacting the ability of operators to operate spent fuel pool cooling, RHR shutdown cooling, and/or ADHR system. Furthermore, the inspectors conducted several walkdowns of the ADHR system during operation with the fuel pool gates removed.
 
Critical Outage Activities The inspectors examined outage activities to verify that they were conducted in accordance with TS, licensee procedures, and the licensee's outage risk control plan. Some of the more significant inspection activities accomplished by the inspectors were as follows:
18 Enclosure
18 Enclosure
* Reviewed and walked down selected safety-related equipment clearance orders (e.g., Equipment Clearance Order 0-TO-2009-0001, Clearance 0-067-0010, for Cutout and Replacement of 1-SHV-67-655, North Header Supply to NE Core Spray Room Cooler).
* Reviewed and walked down selected safety-related equipment clearance orders (e.g., Equipment Clearance Order 0-TO-2009-0001, Clearance 0-067-0010, for Cutout and Replacement of 1-SHV-67-655, North Header Supply to NE Core Spray Room Cooler).
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* Reviewed control of containment penetrations and overall integrity
* Reviewed control of containment penetrations and overall integrity
* Examined foreign material exclusion controls particularly in proximity to and around the reactor cavity, equipment pit, and spent fuel pool
* Examined foreign material exclusion controls particularly in proximity to and around the reactor cavity, equipment pit, and spent fuel pool
* Conducted tours of the MCR, reactor building, refueling floor and drywell     Reactor Vessel Disassembly and Refueling Activities The inspectors witnessed selected activities associated with reactor vessel disassembly, and reactor cavity flood-up and drain down in accordance with 2-GOI-100-3A, Refueling Operations (Reactor Vessel Disassembly and Floodup). Also, on numerous occasions, the inspectors witnessed fuel handling operations during the three Unit 2 reactor core fuel shuffles performed in accordance with TS and applicable operating procedures, such as GOI-100-3A, Refueling Operations (In Vessel), GOI-100-3B, Operations in the Spent Fuel Pool, and GOI-100-3C, Fuel Movement Operations During Refueling. The inspectors verified specific fuel movements as delineated by the Fuel Assembly Transfer Sheets (FATF).
* Conducted tours of the MCR, reactor building, refueling floor and drywell Reactor Vessel Disassembly and Refueling Activities The inspectors witnessed selected activities associated with reactor vessel disassembly, and reactor cavity flood-up and drain down in accordance with 2-GOI-100-3A, Refueling Operations (Reactor Vessel Disassembly and Floodup). Also, on numerous occasions, the inspectors witnessed fuel handling operations during the three Unit 2 reactor core fuel shuffles performed in accordance with TS and applicable operating procedures, such as GOI-100-3A, Refueling Operations (In Vessel), GOI-100-3B, Operations in the Spent Fuel Pool, and GOI-100-3C, Fuel Movement Operations During Refueling. The inspectors verified specific fuel movements as delineated by the Fuel Assembly Transfer Sheets (FATF).


Torus and Drywell Closeout On May 30, the inspectors reviewed the licensee's final closure of the Unit 2 suppression pool in accordance with 2-GOI-200-2, Primary Containment Initial Entry and Closeout, and performed an independent detailed closeout inspection of the Unit 2 torus.
Torus and Drywell Closeout On May 30, the inspectors reviewed the licensee's final closure of the Unit 2 suppression pool in accordance with 2-GOI-200-2, Primary Containment Initial Entry and Closeout, and performed an independent detailed closeout inspection of the Unit 2 torus.


The inspectors conducted several independent detailed closeout inspections of the Unit 2 drywell prior to and ending on June 19. The inspectors also reviewed and verified the licensee's conduct of 2-GOI-200-2.
The inspectors conducted several independent detailed closeout inspections of the Unit 2 drywell prior to and ending on June 19. The inspectors also reviewed and verified the licensee's conduct of 2-GOI-200-2.


Restart Activities The inspectors specifically conducted the following:   - Attended the restart Plant Oversight Review Committee meetings  - Witnessed heatup and pressurization of Unit 2 reactor pressure vessel in accordance with 2-SI-3.3.1.A, ASME Section XI System Leakage Test of the Reactor pressure Vessel and Associated Piping  - Reviewed and verified completion of selected items of 0-TI-270, Refueling Test Program, Attachment 2, Startup Review Checklist 19 Enclosure - Reviewed 2-SR-3.6.1.1.1(OPT-A) Primary Containment Total Leak Rate - Option A, Revision 6  - Witnessed Unit 2 criticality and/or power ascension per 2-GOI-100-1A, Unit Startup and Power Operation, for the startups on June 8, 15, and 20. Also witnessed the Unit 2 shutdowns on June 11 and 16.  - Witnessed and reviewed Unit 2 RCS heatup and pressurization per 2-SR-3.4.9.1, Reactor Heatup and Cooldown Rate Monitoring, for the startups conducted on June 8, 15, and 20. Also witnessed the subsequent RCS cooldowns following the shutdowns on June 11 and 16.
Restart Activities The inspectors specifically conducted the following:
- Attended the restart Plant Oversight Review Committee meetings  
  - Witnessed heatup and pressurization of Unit 2 reactor pressure vessel in accordance with 2-SI-3.3.1.A, ASME Section XI System Leakage Test of the Reactor pressure Vessel and Associated Piping  
   - Reviewed and verified completion of selected items of 0-TI-270, Refueling Test Program, Attachment 2, Startup Review Checklist  


Corrective Action Program The inspectors reviewed PERs generated during U2C15 and attended PER Screening Committee and Corrective Action Review Board meetings to verify that initiation thresholds, priorities, mode holds, operability concerns and significance levels were adequately addressed. Resolution and implementation of corrective actions of several PERs were also reviewed for completeness.
19 Enclosure - Reviewed 2-SR-3.6.1.1.1(OPT-A) Primary Containment Total Leak Rate - Option A, Revision 6
- Witnessed Unit 2 criticality and/or power ascension per 2-GOI-100-1A, Unit Startup and Power Operation, for the startups on June 8, 15, and 20. Also witnessed the Unit 2 shutdowns on June 11 and 16.
 
- Witnessed and reviewed Unit 2 RCS heatup and pressurization per 2-SR-3.4.9.1, Reactor Heatup and Cooldown Rate Monitoring, for the startups conducted on June 8, 15, and 20. Also witnessed the subsequent RCS cooldowns following the shutdowns on June 11 and 16.
 
Corrective Action Program The inspectors reviewed PERs generated during U2C15 and attended PER Screening Committee and Corrective Action Review Board meetings to verify that initiation thresholds, priorities, mode holds, operability concerns and significance levels were adequately addressed. Resolution and implementation of corrective actions of several PERs were also reviewed for completeness.


====b. Findings====
====b. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors witnessed portions and/or reviewed completed test data for the following five surveillance tests of risk-significant and/or safety-related systems to verify that the tests met TS surveillance requirements, UFSAR commitments, and in-service testing and licensee procedure requirements. The inspectors' review confirmed whether the testing effectively demonstrated that the SSCs were operationally capable of performing their intended safety functions and fulfilled the intent of the associated surveillance requirement. In-Service Tests:
The inspectors witnessed portions and/or reviewed completed test data for the following five surveillance tests of risk-significant and/or safety-related systems to verify that the tests met TS surveillance requirements, UFSAR commitments, and in-service testing and licensee procedure requirements. The inspectors' review confirmed whether the testing effectively demonstrated that the SSCs were operationally capable of performing their intended safety functions and fulfilled the intent of the associated surveillance requirement.
* 1-SR-3.5.1.6(CS I), Quarterly CS System Flow Rate Test Loop I   Routine Surveillance Tests:
 
In-Service Tests:
* 1-SR-3.5.1.6(CS I), Quarterly CS System Flow Rate Test Loop I Routine Surveillance Tests
:
* 0-SR-3.8.1.9(D), Diesel Generator D Emergency Unit 2 Load Acceptance Test
* 0-SR-3.8.1.9(D), Diesel Generator D Emergency Unit 2 Load Acceptance Test
* 2-SR-3.1.4.1, Scram Insertion Times
* 2-SR-3.1.4.1, Scram Insertion Times
* 2-SR-3.4.3.2,  Main Steam Relief Valve Manual Cycle Test   Containment Isolation Valve Tests:
* 2-SR-3.4.3.2,  Main Steam Relief Valve Manual Cycle Test Containment Isolation Valve Tests
* 2-SI-4.7.A.2.a-f,  Primary Containment Integrated Leak Rate Test 20 Enclosure
:
* 2-SI-4.7.A.2.a-f,  Primary Containment Integrated Leak Rate Test
 
20 Enclosure


====b. Findings====
====b. Findings====
No findings of significance were identified. Cornerstone: Emergency Preparedness 1EP6 Drill Evaluation
No findings of significance were identified.
 
===Cornerstone:===
Emergency Preparedness 1EP6 Drill Evaluation


====a. Inspection Scope====
====a. Inspection Scope====
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===Cornerstone:===
===Cornerstone:===
Occupational Radiation Safety (OS) 2OS1 Access Control To Radiologically Significant Areas
Occupational Radiation Safety (OS)2OS1 Access Control To Radiologically Significant Areas


====a. Inspection Scope====
====a. Inspection Scope====
Access Control: The inspectors evaluated licensee performance in controlling worker access to radiologically significant areas and monitoring jobs in-progress associated with the U2C15 refueling outage. The inspectors directly observed implementation of administrative and physical radiological controls; evaluated radiation worker (radworker)and radiation protection technician (RPT) knowledge of and proficiency in implementing radiation protection requirements; and assessed worker exposures to radiation and radioactive material. During facility tours, the inspectors directly observed postings and physical controls for radiation areas, high radiation areas (HRAs), and potential airborne radioactivity areas  established within the radiation control area (RCA) of the Unit 2 (U2) drywell, Unit 1 (U1),
Access Control: The inspectors evaluated licensee performance in controlling worker access to radiologically significant areas and monitoring jobs in-progress associated with the U2C15 refueling outage. The inspectors directly observed implementation of administrative and physical radiological controls; evaluated radiation worker (radworker)and radiation protection technician (RPT) knowledge of and proficiency in implementing radiation protection requirements; and assessed worker exposures to radiation and radioactive material.
U2, and Unit 3 (U3) reactor buildings, U1/U2/U3 turbine building, and radioactive waste (radwaste) processing and storage locations. The inspectors independently measured radiation dose rates or directly observed conduct of licensee radiation surveys for selected RCA areas. Results were compared to current licensee surveys and assessed against established postings and Radiation Work Permit (RWP) controls. Licensee key control and access barrier effectiveness were evaluated for selected U1, U2, and U3 21 Enclosure Locked High Radiation Area (LHRA) and Very High Radiation Area (VHRA) locations. Changes to procedural guidance for LHRA and VHRA controls were discussed with radiation protection (RP) supervisors. Controls and their implementation for storage of irradiated material within the spent fuel pool (SFP) were reviewed and discussed in detail. Established radiological controls were evaluated for selected U2C15 outage tasks including transverse in-core probe under-vessel work, control rod drive accumulator maintenance, diving activities associated with steam dryer work, in-service inspection, scaffolding support, insulation, shielding, motor replacements  In addition, licensee controls for areas where dose rates could change significantly as a result of plant shutdown and refueling operations were reviewed and discussed. For selected tasks, the inspectors attended pre-job briefings and reviewed RWP details to assess communication of radiological control requirements to workers. Occupational workers' adherence to selected RWPs and RPT proficiency in providing job coverage were evaluated through direct observations and interviews with licensee staff. Electronic dosimeter (ED) alarm set points and worker stay times were evaluated against area radiation survey results for drywell and refueling floor activities. The inspectors evaluated the effectiveness of radiation exposure controls, including air sampling, barrier integrity, engineering controls, and postings through a review of both internal and external exposure results. Worker exposure as measured by ED and by licensee evaluations of skin doses resulting from discrete radioactive particle or dispersed skin contamination events during current U2C15 outage activities were reviewed and assessed. For HRA tasks involving significant dose rate gradients, e.g. steam dryer repair activities by divers in the fuel pool, the inspectors evaluated the use and placement of whole body and extremity dosimetry to monitor worker exposure. The inspectors also reviewed and discussed selected whole-body count analyses conducted during 2008 and the current U2 refueling outage.
 
During facility tours, the inspectors directly observed postings and physical controls for radiation areas, high radiation areas (HRAs), and potential airborne radioactivity areas  established within the radiation control area (RCA) of the Unit 2 (U2) drywell, Unit 1 (U1),
U2, and Unit 3 (U3) reactor buildings, U1/U2/U3 turbine building, and radioactive waste (radwaste) processing and storage locations. The inspectors independently measured radiation dose rates or directly observed conduct of licensee radiation surveys for selected RCA areas. Results were compared to current licensee surveys and assessed against established postings and Radiation Work Permit (RWP) controls. Licensee key control and access barrier effectiveness were evaluated for selected U1, U2, and U3 21 Enclosure Locked High Radiation Area (LHRA) and Very High Radiation Area (VHRA) locations. Changes to procedural guidance for LHRA and VHRA controls were discussed with radiation protection (RP) supervisors.
 
Controls and their implementation for storage of irradiated material within the spent fuel pool (SFP) were reviewed and discussed in detail. Established radiological controls were evaluated for selected U2C15 outage tasks including transverse in-core probe under-vessel work, control rod drive accumulator maintenance, diving activities associated with steam dryer work, in-service inspection, scaffolding support, insulation, shielding, motor replacements  In addition, licensee controls for areas where dose rates could change significantly as a result of plant shutdown and refueling operations were reviewed and discussed.
 
For selected tasks, the inspectors attended pre-job briefings and reviewed RWP details to assess communication of radiological control requirements to workers. Occupational workers' adherence to selected RWPs and RPT proficiency in providing job coverage were evaluated through direct observations and interviews with licensee staff. Electronic dosimeter (ED) alarm set points and worker stay times were evaluated against area radiation survey results for drywell and refueling floor activities.
 
The inspectors evaluated the effectiveness of radiation exposure controls, including air sampling, barrier integrity, engineering controls, and postings through a review of both internal and external exposure results. Worker exposure as measured by ED and by licensee evaluations of skin doses resulting from discrete radioactive particle or dispersed skin contamination events during current U2C15 outage activities were reviewed and assessed. For HRA tasks involving significant dose rate gradients, e.g. steam dryer repair activities by divers in the fuel pool, the inspectors evaluated the use and placement of whole body and extremity dosimetry to monitor worker exposure. The inspectors also reviewed and discussed selected whole-body count analyses conducted during 2008 and the current U2 refueling outage.


The inspectors walked-down the Independent Spent Fuel Storage Installation (ISFSI) facility, observing the physical condition of the casks, radiological postings, and barriers. The inspectors performed independent gamma radiation surveys of the area and reviewed gamma radiation surveys of the ISFSI facility performed by licensee personnel. Inspectors compared the independent survey results to previous surveys and against procedural and TS limits. The inspectors evaluated implementation of radiological controls, including labeling and posting, and discussed controls with RP staff.
The inspectors walked-down the Independent Spent Fuel Storage Installation (ISFSI) facility, observing the physical condition of the casks, radiological postings, and barriers. The inspectors performed independent gamma radiation surveys of the area and reviewed gamma radiation surveys of the ISFSI facility performed by licensee personnel. Inspectors compared the independent survey results to previous surveys and against procedural and TS limits. The inspectors evaluated implementation of radiological controls, including labeling and posting, and discussed controls with RP staff.
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=====Description:=====
=====Description:=====
On May 15, 2009, a machinist received a briefing on RWP 09270081, U2C15 Reactor Building Movats (Various Dress), with an electronic dosimeter (ED) dose alarm setpoint of 50 millirem (mrem) and a dose rate setpoint of 80 millirem per hour (mrem/hr). Based on the work location communicated to RP by the machinist, he was briefed on the radiological conditions in the HPCI room, located adjacent to the U2 SE Quad on the 519' elevation. The anticipated dose rates in the HPCI room were < 1 mrem/hr general area, with some localized areas < 5 mrem/hr. The RWP required the worker to review appropriate survey data prior to entry and did not allow entry into high radiation areas. The worker then proceeded to the U2 519' SE Quad and, instead of entering the HPCI room, passed through a high radiation area (HRA) swing gate and entered a posted HRA in order to look for the valve he was tasked to work on, located near the RHR pumps. Shortly after entering the HRA, the worker received an unanticipated dose rate alarm of 84 mrem/hr, identified when he logged-off the RWP. Because the worker did not hear the ED alarm, he continued to work in the posted high radiation area, unaware of the radiological conditions because they had not been covered during his briefing.
On May 15, 2009, a machinist received a briefing on RWP 09270081, U2C15 Reactor Building Movats (Various Dress), with an electronic dosimeter (ED) dose alarm setpoint of 50 millirem (mrem) and a dose rate setpoint of 80 millirem per hour (mrem/hr). Based on the work location communicated to RP by the machinist, he was briefed on the radiological conditions in the HPCI room, located adjacent to the U2 SE Quad on the 519' elevation. The anticipated dose rates in the HPCI room were < 1 mrem/hr general area, with some localized areas < 5 mrem/hr. The RWP required the worker to review appropriate survey data prior to entry and did not allow entry into high radiation areas.
 
The worker then proceeded to the U2 519' SE Quad and, instead of entering the HPCI room, passed through a high radiation area (HRA) swing gate and entered a posted HRA in order to look for the valve he was tasked to work on, located near the RHR pumps. Shortly after entering the HRA, the worker received an unanticipated dose rate alarm of 84 mrem/hr, identified when he logged-off the RWP. Because the worker did not hear the ED alarm, he continued to work in the posted high radiation area, unaware of the radiological conditions because they had not been covered during his briefing.


Actual radiological conditions were 30-40 mrem/hr general area, and 50 mrem/hr at 30 cm from the RHR pumps. Based on the briefed radiological conditions, it was expected that the worker would receive 1-2 mrem to perform the valve work; because he performed the work in a significantly higher dose rate field than had been briefed, he received a total dose of 19 mrem.
Actual radiological conditions were 30-40 mrem/hr general area, and 50 mrem/hr at 30 cm from the RHR pumps. Based on the briefed radiological conditions, it was expected that the worker would receive 1-2 mrem to perform the valve work; because he performed the work in a significantly higher dose rate field than had been briefed, he received a total dose of 19 mrem.


The machinist had successfully completed radworker training, which detailed the different types of radiological postings/barriers and requirements for entry into areas such as HRAs. Because a swing gate served as a physical barrier to inadvertent entry into the HRA on the U2 519' SE Quad, the worker missed an opportunity to self-check his actions prior to entry into the area.  
The machinist had successfully completed radworker training, which detailed the different types of radiological postings/barriers and requirements for entry into areas such as HRAs. Because a swing gate served as a physical barrier to inadvertent entry into the HRA on the U2 519' SE Quad, the worker missed an opportunity to self-check his actions prior to entry into the area.


=====Analysis:=====
=====Analysis:=====
The inspectors determined that the failure to follow the requirements of RWP 09270081 was a performance deficiency. This finding was greater than minor because it was associated with the Occupational Radiation Safety Cornerstone attribute of Program and Process (Exposure Control) and adversely affected the cornerstone objective of ensuring adequate protection of worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation.
The inspectors determined that the failure to follow the requirements of RWP 09270081 was a performance deficiency. This finding was greater than minor because it was associated with the Occupational Radiation Safety Cornerstone attribute of Program and Process (Exposure Control) and adversely affected the cornerstone objective of ensuring adequate protection of worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation.


23 Enclosure The finding was evaluated using the Occupational Radiation Safety SDP and determined to be of very low safety significance (Green) because it was not related to As Low As Reasonably Achievable (ALARA) planning, nor did it involve an overexposure or substantial potential for overexposure, and the ability to assess dose was not compromised. The cause of this finding was directly related to the cross-cutting aspect of work practices in the Human Performance area, because the machinist failed to use self-checking prior to passing through the swing gate into the posted high radiation area (H.4.a).  
23 Enclosure The finding was evaluated using the Occupational Radiation Safety SDP and determined to be of very low safety significance (Green) because it was not related to As Low As Reasonably Achievable (ALARA) planning, nor did it involve an overexposure or substantial potential for overexposure, and the ability to assess dose was not compromised. The cause of this finding was directly related to the cross-cutting aspect of work practices in the Human Performance area, because the machinist failed to use self-checking prior to passing through the swing gate into the posted high radiation area (H.4.a).


=====Enforcement:=====
=====Enforcement:=====
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====a. Inspection Scope====
====a. Inspection Scope====
As Low As Reasonably Achievable: The inspectors evaluated ALARA program guidance and implementation for ongoing tasks associated with the U2C15 refueling outage. In addition, the inspectors evaluated the post-outage ALARA activities associated with the Unit 1 Cycle 7 (U1C7) refueling outage. The inspectors reviewed and discussed with licensee staff various ALARA work plan documents, including dose estimates and prescribed ALARA controls for selected outage work activities expected to incur significant collective doses. The inspectors reviewed the implementation of dose-reduction initiatives for high person-rem expenditure tasks. The inspectors evaluated these elements of the ALARA program for consistency with the methods and practices delineated in applicable licensee procedures. The inspectors evaluated the implementation and effectiveness of ALARA planning and program initiatives during work in progress. The inspectors made direct field observations of U2 work activities involving the steam dryer repair, specifically diving operations including diver preparation, supervision, dosimetry placement and removal, and work area radiation surveys. The inspectors observed work on the CRD accumulators, scaffold erection, and in-service inspection. The inspectors interviewed radiation workers and RPT staff to assess their understanding of dose reduction initiatives and their current and expected final accumulated occupational doses at completion of the task.
As Low As Reasonably Achievable: The inspectors evaluated ALARA program guidance and implementation for ongoing tasks associated with the U2C15 refueling outage. In addition, the inspectors evaluated the post-outage ALARA activities associated with the Unit 1 Cycle 7 (U1C7) refueling outage. The inspectors reviewed and discussed with licensee staff various ALARA work plan documents, including dose estimates and prescribed ALARA controls for selected outage work activities expected to incur significant collective doses. The inspectors reviewed the implementation of dose-reduction initiatives for high person-rem expenditure tasks. The inspectors evaluated these elements of the ALARA program for consistency with the methods and practices delineated in applicable licensee procedures.
 
The inspectors evaluated the implementation and effectiveness of ALARA planning and program initiatives during work in progress. The inspectors made direct field observations of U2 work activities involving the steam dryer repair, specifically diving operations including diver preparation, supervision, dosimetry placement and removal, and work area radiation surveys. The inspectors observed work on the CRD accumulators, scaffold erection, and in-service inspection. The inspectors interviewed radiation workers and RPT staff to assess their understanding of dose reduction initiatives and their current and expected final accumulated occupational doses at completion of the task.


24 Enclosure Projected RWP dose expenditure estimates from U2C15 and U1C7 refueling outage efforts were compared to actual dose expenditures, and noted differences were discussed with cognizant ALARA staff. Changes to dose budgets relative to changes in job scope were identified and discussed. The inspectors attended pre-job briefings and evaluated the communication of ALARA goals, RWP requirements, and industry lessons-learned to job crew personnel.
24 Enclosure Projected RWP dose expenditure estimates from U2C15 and U1C7 refueling outage efforts were compared to actual dose expenditures, and noted differences were discussed with cognizant ALARA staff. Changes to dose budgets relative to changes in job scope were identified and discussed. The inspectors attended pre-job briefings and evaluated the communication of ALARA goals, RWP requirements, and industry lessons-learned to job crew personnel.
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The inspectors evaluated the implementation and effectiveness of selected program initiatives with respect to source-term reduction. The inspectors reviewed source term reduction plan that would duplicate many of the source term reduction efforts that have been applied to Unit 1 for the other two units. The inspectors noted that many items in the source term reduction plan had been eliminated or deferred past calendar year (CY) 2014 into the next 5-year planning cycle. The inspectors discussed the potential impacts of the eliminations and deferrals with RP management. The effectiveness of selected shielding packages installed for the current outage was assessed through completion of independent radiation surveys and comparison to applicable licensee survey records and expected planning data.
The inspectors evaluated the implementation and effectiveness of selected program initiatives with respect to source-term reduction. The inspectors reviewed source term reduction plan that would duplicate many of the source term reduction efforts that have been applied to Unit 1 for the other two units. The inspectors noted that many items in the source term reduction plan had been eliminated or deferred past calendar year (CY) 2014 into the next 5-year planning cycle. The inspectors discussed the potential impacts of the eliminations and deferrals with RP management. The effectiveness of selected shielding packages installed for the current outage was assessed through completion of independent radiation surveys and comparison to applicable licensee survey records and expected planning data.


The plant collective exposure histories for CY 2005, 2006 and 2007, taken from data reported to the NRC pursuant to 10 CFR 20.2206(c), were reviewed and discussed with licensee staff, as were established goals for reducing collective exposure. The inspectors reviewed the applicable guidance and examined dose records of declared pregnant workers during CY 2007 and 2008 to evaluate current gestation doses for declared pregnant workers. ALARA activities were evaluated against the requirements specified in 10 CFR 19.12; 10 CFR Part 20, Subparts B, C, F, G, H, and J; and approved licensee procedures. In addition, licensee performance was evaluated against RG 8.8, Information Relevant to Ensuring that Occupational Radiation Exposures at Nuclear Power Stations will be As Low As Reasonably Achievable, and RG 8.13, Instruction Concerning Prenatal Radiation Exposure. Procedures and records reviewed within this inspection area are listed in Sections 2OS1 and 2OS2 of the report Attachment.
The plant collective exposure histories for CY 2005, 2006 and 2007, taken from data reported to the NRC pursuant to 10 CFR 20.2206(c), were reviewed and discussed with licensee staff, as were established goals for reducing collective exposure. The inspectors reviewed the applicable guidance and examined dose records of declared pregnant workers during CY 2007 and 2008 to evaluate current gestation doses for declared pregnant workers.


Problem Identification and Resolution:  The inspectors reviewed the licensee corrective action documents associated with ALARA activities. The inspectors evaluated the licensee's ability to identify, characterize, prioritize, and resolve the identified issues in accordance with the corrective action program. Specific self-assessments, audits, and PERs reviewed and evaluated in detail for this inspection area are identified in Section 2OS2 of the report Attachment. The inspectors completed the 15 required line-item samples and 14 optional line-item samples, for a total of 29 line-item samples, as described in IP 71121.02.
ALARA activities were evaluated against the requirements specified in 10 CFR 19.12; 10 CFR Part 20, Subparts B, C, F, G, H, and J; and approved licensee procedures. In addition, licensee performance was evaluated against RG 8.8, Information Relevant to Ensuring that Occupational Radiation Exposures at Nuclear Power Stations will be As Low As Reasonably Achievable, and RG 8.13, Instruction Concerning Prenatal Radiation Exposure. Procedures and records reviewed within this inspection area are listed in Sections 2OS1 and 2OS2 of the report Attachment.
 
Problem Identification and Resolution:  The inspectors reviewed the licensee corrective action documents associated with ALARA activities. The inspectors evaluated the licensee's ability to identify, characterize, prioritize, and resolve the identified issues in accordance with the corrective action program. Specific self-assessments, audits, and PERs reviewed and evaluated in detail for this inspection area are identified in Section 2OS2 of the report Attachment.
 
The inspectors completed the 15 required line-item samples and 14 optional line-item samples, for a total of 29 line-item samples, as described in IP 71121.02.


====b. Findings====
====b. Findings====
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===Cornerstone:===
===Cornerstone:===
Public Radiation Safety 2PS1 Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems
Public Radiation Safety 2PS1 Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems


====a. Inspection Scope====
====a. Inspection Scope====
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====b. Findings====
====b. Findings====
No findings of significance were identified. 2PS2 Radioactive Material Processing and Transportation
No findings of significance were identified.
 
2PS2 Radioactive Material Processing and Transportation


====a. Inspection Scope====
====a. Inspection Scope====
Waste Processing and Characterization:  The inspectors reviewed the plant's solid radioactive waste system description in the UFSAR and process control program (PCP). The most recent radiological effluent release report was reviewed for information on the types and amounts of waste disposed. The scope of the licensee's audit program was reviewed to verify that it met the requirements of 10 CFR 20.1101(c). The inspectors walked down the accessible portions of the liquid and solid radioactive waste processing systems to verify and assess that the current system configuration and operation agreed with the UFSAR and PCP. The use of video cameras to monitor batch tank levels was also discussed with selected radwaste and operations representatives. The inspectors reviewed the radiological operating report for any documented changes to the radwaste processing systems and discussed observations from a walkdown of the systems with selected radwaste and operations representatives.
Waste Processing and Characterization:  The inspectors reviewed the plant's solid radioactive waste system description in the UFSAR and process control program (PCP). The most recent radiological effluent release report was reviewed for information on the types and amounts of waste disposed. The scope of the licensee's audit program was reviewed to verify that it met the requirements of 10 CFR 20.1101(c). The inspectors walked down the accessible portions of the liquid and solid radioactive waste processing systems to verify and assess that the current system configuration and operation agreed with the UFSAR and PCP. The use of video cameras to monitor batch tank levels was also discussed with selected radwaste and operations representatives.
 
The inspectors reviewed the radiological operating report for any documented changes to the radwaste processing systems and discussed observations from a walkdown of the systems with selected radwaste and operations representatives.
 
The inspectors reviewed the plant's process for transferring radioactive resin and sludge discharges into shipping/disposal containers to determine if appropriate waste stream mixing and/or sampling procedures and methodology for waste concentration averaging provided representative samples of the waste product for waste classification purposes. The inspectors reviewed current 10 CFR 61 analysis results and the procedures for obtaining the samples to support the analysis. The scaling factors used for radioactive waste streams and calculations used for determining the amount of hard to detect nuclides were reviewed. The program was reviewed to verify compliance with 10 CFR 61.55-56 and Appendix G of 10 CFR 20.
 
The inspector reviewed the program for provisions that would ensure that the waste stream composition accounted for changes in operational parameters and would remain valid between required periodic updates.
 
26 Enclosure Transportation:  The inspectors observed the preparation and shipment of resin to a vendor facility. The observations included packaging, surveying, labeling, placarding, vehicle checks, driver's briefing and emergency instructions, a review of shipping papers provided to the driver, and licensee final verification of shipment readiness. The inspectors observed two LSA-II type shipments, one involved a cask of dewatered condensate resin and the other was for contaminated plant protective clothing. The inspectors reviewed selected shipping documentation for shipments that had occurred from January 2008 to May 2009. The inspectors reviewed the QA surveillance documentation verifying compliance with the Certificate of Compliance for a Type B package that included dewatered resin. The inspectors observed, interviewed and reviewed the training records of the radwaste workers who were involved in the selected shipments.
 
Transportation program implementation was reviewed against regulations detailed in 10 CFR Part 20, 10 CFR Part 71, 49 CFR Parts 172-178; as well as the guidance provided in NUREG-1608. Training activities were assessed against 49 CFR Part 172 Subpart H. Documents reviewed during the inspection are listed in Section 2PS2 of the report Attachment.


The inspectors reviewed the plant's process for transferring radioactive resin and sludge discharges into shipping/disposal containers to determine if appropriate waste stream mixing and/or sampling procedures and methodology for waste concentration averaging provided representative samples of the waste product for waste classification purposes. The inspectors reviewed current 10 CFR 61 analysis results and the procedures for obtaining the samples to support the analysis. The scaling factors used for radioactive waste streams and calculations used for determining the amount of hard to detect nuclides were reviewed. The program was reviewed to verify compliance with 10 CFR 61.55-56 and Appendix G of 10 CFR 20. The inspector reviewed the program for provisions that would ensure that the waste stream composition accounted for changes in operational parameters and would remain valid between required periodic updates.
Problem Identification and Resolution:  Select PERs and self-assessments were reviewed in detail and discussed with cognizant licensee personnel. The inspectors assessed the licensee's ability to characterize, prioritize, and resolve the identified issues in accordance with licensee procedure SPP-3.1, Corrective Action Program, Rev.


26 Enclosure Transportation:  The inspectors observed the preparation and shipment of resin to a vendor facility. The observations included packaging, surveying, labeling, placarding, vehicle checks, driver's briefing and emergency instructions, a review of shipping papers provided to the driver, and licensee final verification of shipment readiness. The inspectors observed two LSA-II type shipments, one involved a cask of dewatered condensate resin and the other was for contaminated plant protective clothing. The inspectors reviewed selected shipping documentation for shipments that had occurred from January 2008 to May 2009. The inspectors reviewed the QA surveillance documentation verifying compliance with the Certificate of Compliance for a Type B package that included dewatered resin. The inspectors observed, interviewed and reviewed the training records of the radwaste workers who were involved in the selected shipments. Transportation program implementation was reviewed against regulations detailed in 10 CFR Part 20, 10 CFR Part 71, 49 CFR Parts 172-178; as well as the guidance provided in NUREG-1608. Training activities were assessed against 49 CFR Part 172 Subpart H. Documents reviewed during the inspection are listed in Section 2PS2 of the report Attachment. Problem Identification and Resolution:  Select PERs and self-assessments were reviewed in detail and discussed with cognizant licensee personnel. The inspectors assessed the licensee's ability to characterize, prioritize, and resolve the identified issues in accordance with licensee procedure SPP-3.1, Corrective Action Program, Rev.
15. Documents reviewed for problem identification and resolution are listed in Section 2PS2 of the report Attachment.


15. Documents reviewed for problem identification and resolution are listed in Section 2PS2 of the report Attachment. The inspectors completed the six required line-item samples described in IP 71122.02.
The inspectors completed the six required line-item samples described in IP 71122.02.


====b. Findings====
====b. Findings====
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===.1 Cornerstone:===
===.1 Cornerstone:===
Mitigating Systems Safety System Functional Failures
Mitigating Systems Safety System Functional Failures


====a. Inspection Scope====
====a. Inspection Scope====
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===.2 Cornerstone:===
===.2 Cornerstone:===
Occupational Radiation Safety Occupational Exposure Control Effectiveness
Occupational Radiation Safety Occupational Exposure Control Effectiveness


====a. Inspection Scope====
====a. Inspection Scope====
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===.3 Cornerstone:===
===.3 Cornerstone:===
Public Radiation Safety Radiological Control Effluent Release Occurrences
Public Radiation Safety Radiological Control Effluent Release Occurrences


====a. Inspection Scope====
====a. Inspection Scope====
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===.1 Review of items Entered into the Corrective Action Program:===
===.1 Review of items Entered into the Corrective Action Program:===
As required by Inspection Procedure 71152, "Identification and Resolution of Problems," and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensee's CAP. This review was accomplished by reviewing daily PER report summaries, periodically attending Corrective Action Review Board (CARB) meetings and periodically attending PER Screening Committee (PSC) meetings.
As required by Inspection Procedure 71152, "Identification and Resolution of Problems," and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensee's CAP. This review was accomplished by reviewing daily PER report summaries, periodically attending Corrective Action Review Board (CARB) meetings and periodically attending PER Screening Committee (PSC) meetings.


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The inspectors noted areas in the trending program that warranted additional attention by the licensee, as follows:
The inspectors noted areas in the trending program that warranted additional attention by the licensee, as follows:
* Some departmental negative trends that were continuing from previous ITRs relied on existing PERs or were closed to existing programs, without conducting a thorough evaluation if the existing PERs or programs were adequate to correct the problem. For example, several negative trends identified in the radiation protection department (e.g., contaminated area, number of hot spots, number of 29 Enclosure catch containments), were identified and new PERs were written. However, these PERs were closed to existing programs which have not been effective in reversing these trends. It was not apparent that an adequate evaluation was being conducted to ensure that the existing PER corrective actions were being effective, that these actions were timely enough or that criteria was being established where additional actions were needed (i.e., when an additional PER would be required).
* Some departmental negative trends that were continuing from previous ITRs relied on existing PERs or were closed to existing programs, without conducting a thorough evaluation if the existing PERs or programs were adequate to correct the problem. For example, several negative trends identified in the radiation protection department (e.g., contaminated area, number of hot spots, number of 29 Enclosure catch containments), were identified and new PERs were written. However, these PERs were closed to existing programs which have not been effective in reversing these trends. It was not apparent that an adequate evaluation was being conducted to ensure that the existing PER corrective actions were being effective, that these actions were timely enough or that criteria was being established where additional actions were needed (i.e., when an additional PER would be required).
* Department trend reports contained issues identified by external organizations, but in general did not address why the line organization did not identify these issues as required by PIDP-11. The licensee initiated PER 171857. The inspectors conducted an independent review to identify potential negative trends, and identified several notable trends, as follows:
* Department trend reports contained issues identified by external organizations, but in general did not address why the line organization did not identify these issues as required by PIDP-11. The licensee initiated PER 171857.
 
The inspectors conducted an independent review to identify potential negative trends, and identified several notable trends, as follows:
* A potential adverse trend was identified in conducting adequate PMTs. Some examples included: Unit 2 HPCI steam admission valve was repaired to correct seat leakage, but no seat leakage PMT was conducted (PER 161154); RHR HX outlet valves exhibited high vibrations causing repetitive failures, but following replacement of these valves vibration levels are not measured or evaluated (PER 171914); EECW manual isolation valve was replaced, but adequate flow to the room cooler was not verified during the PMT (PER 170650); and pressure testing following replacement of a manual isolation valve in the control rod drive system was not conducting at normal operating pressure (PER 172233). The licensee initiated PER 173055 to address this trend.
* A potential adverse trend was identified in conducting adequate PMTs. Some examples included: Unit 2 HPCI steam admission valve was repaired to correct seat leakage, but no seat leakage PMT was conducted (PER 161154); RHR HX outlet valves exhibited high vibrations causing repetitive failures, but following replacement of these valves vibration levels are not measured or evaluated (PER 171914); EECW manual isolation valve was replaced, but adequate flow to the room cooler was not verified during the PMT (PER 170650); and pressure testing following replacement of a manual isolation valve in the control rod drive system was not conducting at normal operating pressure (PER 172233). The licensee initiated PER 173055 to address this trend.
* The licensee established a PER corrective action closure review committee to ensure that corrective actions were being completed as described in the original action statement and properly documented. Over 70 PERs have been generated by this committee to document problems with PER action closures. In general, these PERs corrected the specific condition described, but no trend PER has been generated to evaluate and correct this trend in inappropriate approval of inadequate PER actions. The licensee initiated PER 175822 to address this trend.
* The licensee established a PER corrective action closure review committee to ensure that corrective actions were being completed as described in the original action statement and properly documented. Over 70 PERs have been generated by this committee to document problems with PER action closures. In general, these PERs corrected the specific condition described, but no trend PER has been generated to evaluate and correct this trend in inappropriate approval of inadequate PER actions. The licensee initiated PER 175822 to address this trend.
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=====Introduction:=====
=====Introduction:=====
The inspectors identified an issue associated with the possible omission of certain risk significant systems from the licensee's routine assessment of online risk that was required by 10 CFR Part 50.65 (a)(4), "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants."  This issue is being characterized as an unresolved item (URI).
The inspectors identified an issue associated with the possible omission of certain risk significant systems from the licensee's routine assessment of online risk that was required by 10 CFR Part 50.65 (a)(4), "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants.
 
"  This issue is being characterized as an unresolved item (URI).


=====Description:=====
=====Description:=====
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This issue of concern requires additional information from the licensee. Such as, whether the MR and Table 2 designations of risk significant systems are appropriate, and how the current online risk assessment tools do or do not scope or bound the impact on risk associated with the unavailability of the aforementioned systems. Consequently, pending additional information from the licensee and further review by the NRC, this issue will be identified as URI 05000259, 260, 296/2009003-04, Inadequate Scoping of Risk Significant Systems for Online Risk Assessment.
This issue of concern requires additional information from the licensee. Such as, whether the MR and Table 2 designations of risk significant systems are appropriate, and how the current online risk assessment tools do or do not scope or bound the impact on risk associated with the unavailability of the aforementioned systems. Consequently, pending additional information from the licensee and further review by the NRC, this issue will be identified as URI 05000259, 260, 296/2009003-04, Inadequate Scoping of Risk Significant Systems for Online Risk Assessment.


Observations The inspectors had the following observations: PERs 160566, 167965, and 170977 31 Enclosure The evaluation, development, and implementation of corrective actions for inadequate communications of plant risk were untimely and remained incomplete. As a potential adverse trend, this issue was discussed with the licensee in December 2008 and documented in NRC Integrated Inspection Report 05000259/2008005, 05000260/2008005 and 05000296/2008005, issued in January 2009. The licensee initiated PER 160566 on January 8, 2009 to document this potential trend in plant risk management where there were numerous instances in which risk assessments from ORAM, the shutdown plant outage risk assessment management software, and SENTINEL, the operating plant computer based risk management model, did not accurately reflect the actual plant equipment configuration. The corrective action to evaluate the potential trend was initiated on February 6, 2009. Subsequently, the licensee extended the PER citing resource re-allocation due to unplanned forced outages. On April 7, 2009, the licensee determined that a trend existed for not meeting expectations for clear communications of plant risk such as:  conflicting risk levels on different site documents; incorrect information related to equipment out of service in the plan of the day; and inadequate transition from ORAM to SENTINEL risk model during unit restart. On that same day, PER 167965 was initiated to develop a corrective action plan for this trend. On May 6, 2009, PER 167965 was prematurely closed with incomplete actions taken, contrary to actions previously discussed with NRC inspectors. On May 11, 2009, the licensee initiated a third PER 170977 to document additional corrective actions. Inspectors discussed their concern with further prolonging corrective actions and the licensee initiated PER 171722 for inadequate and untimely corrective actions.
Observations The inspectors had the following observations:
PERs 160566, 167965, and 170977


SPP-7.3, Work Activity Risk Management Process Inspectors reviewed newly developed licensee procedure SPP-7.3, Work Activity Risk Management Process, to evaluate the corrective actions documented in PER 167965.
31 Enclosure The evaluation, development, and implementation of corrective actions for inadequate communications of plant risk were untimely and remained incomplete. As a potential adverse trend, this issue was discussed with the licensee in December 2008 and documented in NRC Integrated Inspection Report 05000259/2008005, 05000260/2008005 and 05000296/2008005, issued in January 2009. The licensee initiated PER 160566 on January 8, 2009 to document this potential trend in plant risk management where there were numerous instances in which risk assessments from ORAM, the shutdown plant outage risk assessment management software, and SENTINEL, the operating plant computer based risk management model, did not accurately reflect the actual plant equipment configuration. The corrective action to evaluate the potential trend was initiated on February 6, 2009. Subsequently, the licensee extended the PER citing resource re-allocation due to unplanned forced outages. On April 7, 2009, the licensee determined that a trend existed for not meeting expectations for clear communications of plant risk such as:  conflicting risk levels on different site documents; incorrect information related to equipment out of service in the plan of the day; and inadequate transition from ORAM to SENTINEL risk model during unit restart. On that same day, PER 167965 was initiated to develop a corrective action plan for this trend. On May 6, 2009, PER 167965 was prematurely closed with incomplete actions taken, contrary to actions previously discussed with NRC inspectors. On May 11, 2009, the licensee initiated a third PER 170977 to document additional corrective actions. Inspectors discussed their concern with further prolonging corrective actions and the licensee initiated PER 171722 for inadequate and untimely corrective actions.
 
SPP-7.3, Work Activity Risk Management Process Inspectors reviewed newly developed licensee procedure SPP-7.3, Work Activity Risk Management Process, to evaluate the corrective actions documented in PER 167965.


The inspectors made the following observations:
The inspectors made the following observations:
* The relocation of risk management action (RMA) guidance from SPP-7.1, On-Line Work Management, to SPP-7.3 was incomplete. SPP-7.3, Appendix E lists RMAs available for various levels of risk, but did not include all of the RMAs in SPP-7.1, Section 3.5.1.c. Additionally, SPP-7.1, Appendix J contained critical evolution meeting guidance that in itself was an RMA, and was not contained in SPP-7.3. The licensee's site and corporate (SPP administrators) personnel agreed with inspector observations and intend to revise the two SPPs in accordance with their corporate procedure process.
* The relocation of risk management action (RMA) guidance from SPP-7.1, On-Line Work Management, to SPP-7.3 was incomplete. SPP-7.3, Appendix E lists RMAs available for various levels of risk, but did not include all of the RMAs in SPP-7.1, Section 3.5.1.c. Additionally, SPP-7.1, Appendix J contained critical evolution meeting guidance that in itself was an RMA, and was not contained in SPP-7.3. The licensee's site and corporate (SPP administrators) personnel agreed with inspector observations and intend to revise the two SPPs in accordance with their corporate procedure process.
* Risk management review forms to support the new SPP-7.3 procedure had still not been developed four weeks after the procedure became effective. The licensee stated that implementation of the procedure was planned to be a phased-in effort coinciding with the work week development process, and initiated an action as part of PER 170977 to track the development of the forms. BP-336, Risk Determination and Risk Management With approximately 11 weeks remaining until BP-336 would be phased out and deactivated, inspectors noted that Operations guidance associated with plant risk matrices and protected equipment (which the operations department intended to maintain) did not have a prospective home in another procedure or similar guidance 32 Enclosure document. Inspectors also noted that the licensee had not documented this concern in their CAP, and therefore a documented plan of action was not in place. The licensee initiated an action as part of PER 170977. Equipment Out of Service (EOOS) Risk Assessment Tool During discussions with the licensee concerning their development of new risk management and assessment tools, inspectors noted that with the planned phasing in of the new PRA-based EOOS software near the end of 2009 and the planned phasing out of SENTINEL, there was a lack of risk assessment tool coverage for Mode 3 Hot Shutdown. The licensee agreed that this would be the case until the low power shutdown model was completed in approximately five years which would apply in Modes 1, 2, and 3. The licensee initiated PER 169925 to resolve risk tool coverage for Mode 3 conditions.  
* Risk management review forms to support the new SPP-7.3 procedure had still not been developed four weeks after the procedure became effective. The licensee stated that implementation of the procedure was planned to be a phased-in effort coinciding with the work week development process, and initiated an action as part of PER 170977 to track the development of the forms.
 
BP-336, Risk Determination and Risk Management With approximately 11 weeks remaining until BP-336 would be phased out and deactivated, inspectors noted that Operations guidance associated with plant risk matrices and protected equipment (which the operations department intended to maintain) did not have a prospective home in another procedure or similar guidance 32 Enclosure document. Inspectors also noted that the licensee had not documented this concern in their CAP, and therefore a documented plan of action was not in place. The licensee initiated an action as part of PER 170977.
 
Equipment Out of Service (EOOS) Risk Assessment Tool
 
During discussions with the licensee concerning their development of new risk management and assessment tools, inspectors noted that with the planned phasing in of the new PRA-based EOOS software near the end of 2009 and the planned phasing out of SENTINEL, there was a lack of risk assessment tool coverage for Mode 3 Hot Shutdown. The licensee agreed that this would be the case until the low power shutdown model was completed in approximately five years which would apply in Modes 1, 2, and 3. The licensee initiated PER 169925 to resolve risk tool coverage for Mode 3 conditions.
 
{{a|4OA3}}
{{a|4OA3}}
==4OA3 Event Follow-up==
==4OA3 Event Follow-up==
Line 521: Line 645:


====b. Findings====
====b. Findings====
This LER is considered closed with one finding identified.  
This LER is considered closed with one finding identified.


=====Introduction:=====
=====Introduction:=====
Line 527: Line 651:


=====Description:=====
=====Description:=====
A review of work orders from as far back as 1993, by the licensee, determined that plant personnel frequently observed excessive condensation dripping from the IBC system ductwork during winter operating conditions. Alabama winters have frequently included certain days when river water temperatures were very cold, but ambient air was warm and humid (e.g., after a storm front). During these conditions, the IBC coolers would generate considerable quantities of condensed water in the bus ductwork. Excessive condensation dripping from the IBC ductwork seams had been observed and tolerated by the licensee for many years. In 2006, Unit 1 installed a new IBC system. This new system was designed to have much a higher capacity cooler, along with dual fans vice the original single fan design. The new Unit 1 IBC design was based on the worst case Extended Power Uprate Isophase Bus loading, along with worst case river water temperatures (i.e., during the summer). The licensee determined in their root cause analysis, that the Unit 1 IBC design change did not consider or evaluate the potential adverse implications associated with winter operating conditions. The inspectors verified that the technical considerations required to be evaluated by SPP-9.3, Plant Modifications and Engineering Change Control, for design changes did not require the impact of seasonal environmental changes to be evaluated. However, it was apparent to the licensee and inspectors, that the new design features of the Unit 1 IBC system were more conducive to generating and accumulating larger quantities of condensation during winter operating conditions than the old system. On December 8, 2007, as in previous occasions, plant personnel observed water leaking from the seams of the Unit 1 IBC ductwork and initiated WO 07-727187-000 to correct the problem. However, the WO wasn't worked until October 2008 at which time there was no water to be found. This WO was closed with no work performed. Then, on December 10, 2008, plant personnel again discovered excessive moisture coming out of the seams of the Unit 1 IBC ductwork. This time the abnormal equipment condition was entered into the licensee's CAP as PER 158940 (Level C PER). The inspectors noted that the specific actions to promptly correct the problem recommended by the PER were not implemented prior to the event.
A review of work orders from as far back as 1993, by the licensee, determined that plant personnel frequently observed excessive condensation dripping from the IBC system ductwork during winter operating conditions. Alabama winters have frequently included certain days when river water temperatures were very cold, but ambient air was warm and humid (e.g., after a storm front). During these conditions, the IBC coolers would generate considerable quantities of condensed water in the bus ductwork. Excessive condensation dripping from the IBC ductwork seams had been observed and tolerated by the licensee for many years.
 
In 2006, Unit 1 installed a new IBC system. This new system was designed to have much a higher capacity cooler, along with dual fans vice the original single fan design. The new Unit 1 IBC design was based on the worst case Extended Power Uprate Isophase Bus loading, along with worst case river water temperatures (i.e., during the summer). The licensee determined in their root cause analysis, that the Unit 1 IBC design change did not consider or evaluate the potential adverse implications associated with winter operating conditions. The inspectors verified that the technical considerations required to be evaluated by SPP-9.3, Plant Modifications and Engineering Change Control, for design changes did not require the impact of seasonal environmental changes to be evaluated. However, it was apparent to the licensee and inspectors, that the new design features of the Unit 1 IBC system were more conducive to generating and accumulating larger quantities of condensation during winter operating conditions than the old system. On December 8, 2007, as in previous occasions, plant personnel observed water leaking from the seams of the Unit 1 IBC ductwork and initiated WO 07-727187-000 to correct the problem. However, the WO wasn't worked until October 2008 at which time there was no water to be found. This WO was closed with no work performed. Then, on December 10, 2008, plant personnel again discovered excessive moisture coming out of the seams of the Unit 1 IBC ductwork. This time the abnormal equipment condition was entered into the licensee's CAP as PER 158940 (Level C PER). The inspectors noted that the specific actions to promptly correct the problem recommended by the PER were not implemented prior to the event.


In the purpose section of SPP-3.1, Corrective Action Program, it stated that this SPP established the processes and responsibilities for documenting and resolving problems at the station. This program procedure also addressed safety-related problems required 34 Enclosure to be corrected by 10 CFR 50, Appendix B, Criterion XVI, Corrective Action. The overall purpose of the licensee's CAP was to provide the necessary site standards to ensure that all abnormal equipment conditions entered into the CAP, including non-safety related equipment deficiencies, were resolved. The licensee initiated PER 158940, and designated it as a Level C PER, to ensure that the site standards imposed by SPP-3.1 were implemented and followed to resolve the excessive IBC system condensation. The licensee's failure to implement the actions recommended by PER 158940 in a timely manner was a missed opportunity to prevent the Unit 1 reactor scram of February 18, 2009. During the subsequent event investigation, shortly after the Unit 1 scram, the licensee discovered approximately 35 gallons of water (i.e., condensate) remaining in the IBC ductwork. From this observation and a system walkdown, the licensee concluded that at least this amount of water had originally condensed and collected in the idle 1B IBC fan housing prior to the event. Based on the observed persistent problems with water accumulation in the IBC ductwork, including the multiple WO's and PERs that were written, the inspectors concluded the licensee had many past and recent opportunities to address this condition. It was therefore reasonable to conclude that it was within the licensee's ability to foresee and correct the condition before it resulted in a reactor scram.
In the purpose section of SPP-3.1, Corrective Action Program, it stated that this SPP established the processes and responsibilities for documenting and resolving problems at the station. This program procedure also addressed safety-related problems required 34 Enclosure to be corrected by 10 CFR 50, Appendix B, Criterion XVI, Corrective Action. The overall purpose of the licensee's CAP was to provide the necessary site standards to ensure that all abnormal equipment conditions entered into the CAP, including non-safety related equipment deficiencies, were resolved. The licensee initiated PER 158940, and designated it as a Level C PER, to ensure that the site standards imposed by SPP-3.1 were implemented and followed to resolve the excessive IBC system condensation. The licensee's failure to implement the actions recommended by PER 158940 in a timely manner was a missed opportunity to prevent the Unit 1 reactor scram of February 18, 2009. During the subsequent event investigation, shortly after the Unit 1 scram, the licensee discovered approximately 35 gallons of water (i.e., condensate) remaining in the IBC ductwork. From this observation and a system walkdown, the licensee concluded that at least this amount of water had originally condensed and collected in the idle 1B IBC fan housing prior to the event. Based on the observed persistent problems with water accumulation in the IBC ductwork, including the multiple WO's and PERs that were written, the inspectors concluded the licensee had many past and recent opportunities to address this condition. It was therefore reasonable to conclude that it was within the licensee's ability to foresee and correct the condition before it resulted in a reactor scram.
Line 553: Line 679:


====a. Inspection Scope====
====a. Inspection Scope====
During the inspection period the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security. These observations took place during both normal and off-normal plant working hours. These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status reviews and inspection activities.
During the inspection period the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security. These observations took place during both normal and off-normal plant working hours.
 
These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status reviews and inspection activities.


====b. Findings====
====b. Findings====
No significant findings were identified.  
No significant findings were identified.
 
{{a|4OA6}}
{{a|4OA6}}
==4OA6 Meetings, Including Exit==
==4OA6 Meetings, Including Exit==


===.1 Quarterly Integrated Inspection Report Exit Meeting Summary===
===.1 Quarterly Integrated Inspection Report Exit Meeting Summary===
On July 6 and 17, 2009, the senior resident inspector presented the inspection results to Mr. Jim Randich, Mr. Don Grissette, and other members of the licensee staff, who acknowledged the findings. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary. No proprietary information was identified.
On July 6 and 17, 2009, the senior resident inspector presented the inspection results to Mr. Jim Randich, Mr. Don Grissette, and other members of the licensee staff, who acknowledged the findings. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary. No proprietary information was identified.


Line 566: Line 696:
{{a|4OA7}}
{{a|4OA7}}
==4OA7 Licensee-Identified Violations==
==4OA7 Licensee-Identified Violations==
The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which met the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as a Non-Cited Violation.
The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which met the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as a Non-Cited Violation.
* TS 5.7.1, requires that each individual or group entering such an area (locked high radiation area) shall possess a device that continuously transmits dose rate information to a remote receiver monitored by radiation protection personnel or be under the surveillance of an individual qualified in radiation protection procedures equipped with a radiation monitoring device that continuously displays dose rates in the area. Contrary to this, on April 15, 2008, a radworker retrieved his ED from the 550 foot elevation of the U3 drywell without being issued another ED, being monitored by a RPT or being accompanied by a RPT with a survey instrument. This event was documented in the licensee's CAP as PER 142319. This finding was of very low safety significance because there was no substantial potential for overexposure and the licensee's ability to assess dose was not compromised.
* TS 5.7.1, requires that each individual or group entering such an area (locked high radiation area) shall possess a device that continuously transmits dose rate information to a remote receiver monitored by radiation protection personnel or be under the surveillance of an individual qualified in radiation protection procedures equipped with a radiation monitoring device that continuously displays dose rates in the area. Contrary to this, on April 15, 2008, a radworker retrieved his ED from the 550 foot elevation of the U3 drywell without being issued another ED, being monitored by a RPT or being accompanied by a RPT with a survey instrument. This event was documented in the licensee's CAP as PER 142319. This finding was of very low safety significance because there was no substantial potential for overexposure and the licensee's ability to assess dose was not compromised.
Line 603: Line 734:
: [[contact::J. Underwood]], Site Nuclear Assurance Manager   
: [[contact::J. Underwood]], Site Nuclear Assurance Manager   
: [[contact::J. Walton]], Radiation Protection Supervisor  
: [[contact::J. Walton]], Radiation Protection Supervisor  
: [[contact::R. West]], Site Vice President    
: [[contact::R. West]], Site Vice President  


==LIST OF ITEMS==
==LIST OF ITEMS==
OPENED, CLOSED AND DISCUSSED
 
===OPENED, CLOSED AND DISCUSSED===
 
===Opened===
===Opened===
: 05000259, 260, 296/2009003-04 URI Inadequate Scoping of Risk Significant Systems For Online Risk Assessment (Section 4OA2.3)
: 05000259, 260, 296/2009003-04 URI Inadequate Scoping of Risk Significant Systems For Online Risk Assessment (Section 4OA2.3)  
 
===Opened and Closed===
===Opened and Closed===
: 05000260/2009003-01 NCV Failure to Assess and Manage Shutdown Risk Associated with Outage Maintenance Activities (Section 1R13)
: 05000260/2009003-01 NCV Failure to Assess and Manage Shutdown Risk Associated with Outage Maintenance Activities (Section 1R13)  
: 05000259/2009003-02 NCV Failure to Perform an Adequate Risk Assessment during Severe Weather Conditions (Section 1R13)
: 05000259/2009003-02 NCV Failure to Perform an Adequate Risk Assessment during Severe Weather Conditions (Section 1R13)  
: 05000259, 260, 296/2009003-03 NCV Failure to Comply with the Requirements of an RWP by Entering a Posted High Radiation Area (Section 2OS1)
: 05000259, 260, 296/2009003-03 NCV Failure to Comply with the Requirements of an RWP by Entering a Posted High Radiation Area (Section 2OS1)  
: 05000259/2009003-05 FIN Untimely Actions to Resolve Excessive IBC System Condensation Results in Unit 1 Reactor Scram  
: 05000259/2009003-05 FIN Untimely Actions to Resolve Excessive IBC System Condensation Results in Unit 1 Reactor Scram  
(Section 4OA3.2)
(Section 4OA3.2)  
 
===Closed===
===Closed===
: LER
: 05000260/2009001-00
: LER Manual Reactor Scram Following Stator Cooling Water Equipment Failure (Section 4OA3.1)
: LER
: LER
: [[Closes LER::05000260/LER-2009-001]]-00  LER Manual Reactor Scram Following Stator Cooling Water Equipment Failure (Section 4OA3.1)  LER
: [[Closes LER::05000259/LER-2009-001]]-00  LER Turbine Trip and Reactor Scram Due to Power Load Unbalance Signal on the Main Generator  
: [[Closes LER::05000259/LER-2009-001]]-00  LER Turbine Trip and Reactor Scram Due to Power Load Unbalance Signal on the Main Generator  
(Section 4OA3.2) LER
(Section 4OA3.2)  
: [[Closes LER::05000259/LER-2009-002]]-00  LER Unexpected Logic Lockout of the Loop II Residual Heat Removal System Pumps (Section 4OA3.3)
: LER
: [[Closes LER::05000259/LER-2009-002]]-00  LER Unexpected Logic Lockout of the Loop II Residual Heat Removal System Pumps (Section 4OA3.3)  
 
===Discussed===
===Discussed===
None   
None   
Line 632: Line 771:
: TRO-VP-SPP-10.006, Loss of SCADA and/or EMS, Rev. 3
: TRO-VP-SPP-10.006, Loss of SCADA and/or EMS, Rev. 3
: TRO-TO-SOP-10.128, Browns Ferry Nuclear Plant (BFN) Grid Operating Guide
: TRO-TO-SOP-10.128, Browns Ferry Nuclear Plant (BFN) Grid Operating Guide
: TRO-TO-SOP-10.328, Nuclear Offsite Disqualification Notification and Call-Out Procedure, Rev. 5
: TRO-TO-SOP-10.328, Nuclear Offsite Disqualification Notification and Call-Out Procedure, Rev.


==Section 1R04: Equipment Alignment==
==Section 1R04: Equipment Alignment==
: 2-OI-75 Attachment 1, Core Spray System Valve Lineup Checklist, March 19, 2007 2-OI-75 Attachment 2, Core Spray System Panel Lineup Checklist, March 19, 2007  
: 2-OI-75 Attachment 1, Core Spray System Valve Lineup Checklist, March 19, 2007 2-OI-75 Attachment 2, Core Spray System Panel Lineup Checklist, March 19, 2007  
: 2-OI-75 Attachment 3, Core Spray System Electrical Lineup Checklist, March 19, 2007 Drawing 3-47E812-1, Flow Diagram High Pressure Coolant Injection System 3-OI-74, Residual Heat Removal System, Rev. 86 3-OI-74, Attachment 1, RHR System Valve Lineup Checklist, Rev. 86  
: 2-OI-75 Attachment 3, Core Spray System Electrical Lineup Checklist, March 19, 2007 Drawing 3-47E812-1, Flow Diagram High Pressure Coolant Injection System 3-OI-74, Residual Heat Removal System, Rev. 86
: 3-OI-74, Attachment 1, RHR System Valve Lineup Checklist, Rev. 86  
: 3-OI-74, Attachment 2, RHR System Panel Lineup Checklist, Rev. 86 3-OI-74, Attachment 3, RHR System Electrical Lineup Checklist, Rev. 86 Drawing 3-47E811-1, Flow Diagram Residual Heat Removal System, Rev. 64
: 3-OI-74, Attachment 2, RHR System Panel Lineup Checklist, Rev. 86 3-OI-74, Attachment 3, RHR System Electrical Lineup Checklist, Rev. 86 Drawing 3-47E811-1, Flow Diagram Residual Heat Removal System, Rev. 64


Line 670: Line 810:
: PER 121787, Indication in N9 Nozzle to Vessel Weld, 03/17/2007
: PER 121787, Indication in N9 Nozzle to Vessel Weld, 03/17/2007
: PER 121003, NOI U2C14-017, CRD Weld Indication, 03/06/2007
: PER 121003, NOI U2C14-017, CRD Weld Indication, 03/06/2007
: PER 169585, RHRSW Effluent, 04/26/2009  
: PER 169585, RHRSW Effluent, 04/26/2009
===Procedures===
===Procedures===
: N-VT-1, Rev. 44, Visual Examination Procedure for ASME Section Xi Preservice and Inservice, 04/21/2009 N-PT-9, Rev. 33, Liquid Penetrant Examination of ASME and ANSI Code Components and Welds, 02/18/2009 N-UT-78, Rev. 5, PDI Generic Procedure for the Manual Ultrasonic Examination of Reactor Pressure Vessel Welds
: N-VT-1, Rev. 44, Visual Examination Procedure for ASME Section Xi Preservice and Inservice, 04/21/2009 N-PT-9, Rev. 33, Liquid Penetrant Examination of ASME and ANSI Code Components and Welds, 02/18/2009 N-UT-78, Rev. 5, PDI Generic Procedure for the Manual Ultrasonic Examination of Reactor Pressure Vessel Welds
: PDI-UT-6, 08/11/2008 N-UT-79, Rev. 2, PDI Generic Procedure for the Manual Ultrasonic Through Wall and Length Sizing of Ultrasonic Indications in Reactor Pressure Vessel Welds
: PDI-UT-6, 08/11/2008 N-UT-79, Rev. 2, PDI Generic Procedure for the Manual Ultrasonic Through Wall and Length Sizing of Ultrasonic Indications in Reactor Pressure Vessel Welds
: PDI-UT-7, 08/18/2008 N-UT-84, Rev. 0, Procedure for the Phased Array Ultrasonic Examination of Austenitic and Ferritic Pipe Welds, 10/21/2008 54-ISI-363, Rev. 5, Remote Underwater In-Vessel Visual Inspection of Reactor Pressure Vessel Internals, Components, and Associated Repairs in Boiling Water Reactors, 10/21/2008  
: PDI-UT-7, 08/18/2008 N-UT-84, Rev. 0, Procedure for the Phased Array Ultrasonic Examination of Austenitic and Ferritic Pipe Welds, 10/21/2008 54-ISI-363, Rev. 5, Remote Underwater In-Vessel Visual Inspection of Reactor Pressure Vessel Internals, Components, and Associated Repairs in Boiling Water Reactors, 10/21/2008
===Other Documents===
===Other Documents===
: CRP-ENG-SS-08-005, Snapshot Self-Assessment Report, 04/30/08 Corporate Engineering Welding Assessment Report, 08/03/2004 Browns Ferry Nuclear Plant (BFN) - Unit 2 - American Society of Mechanical Engineers (ASME) Section XI, Inservice Inspection, System Pressure Test, Containment Inspection (IWE), and Repair and Replacement Programs - Summary Reports (NIS-1 and
: CRP-ENG-SS-08-005, Snapshot Self-Assessment Report, 04/30/08 Corporate Engineering Welding Assessment Report, 08/03/2004 Browns Ferry Nuclear Plant (BFN) - Unit 2 - American Society of Mechanical Engineers (ASME) Section XI, Inservice Inspection, System Pressure Test, Containment Inspection (IWE), and Repair and Replacement Programs - Summary Reports (NIS-1 and
Line 729: Line 869:
: BFN-0-09-029
: BFN-0-09-029
: PER 170184, Installation of N-1 Nozzle
: PER 170184, Installation of N-1 Nozzle
: PER 170184, Diesel Removed From Service During Severe Weather
: PER 170184, Diesel Removed From Service During Severe Weather
: ORAM Reports (5/19 and 5/20/09)  
: ORAM Reports (5/19 and 5/20/09)  
: Unit 2 Outage Reports (5/19 and 5/20/09)
: Unit 2 Outage Reports (5/19 and 5/20/09)
Line 760: Line 900:
: MD-Q0001-960036, MSIV Leakage Containment System Boundaries, Physical Boundaries - System 001, Rev. 4
: MD-Q0001-960036, MSIV Leakage Containment System Boundaries, Physical Boundaries - System 001, Rev. 4
: BFN-50-7001, General Design Criteria for Main Steam System, Rev. 23 DCN T41019, Mods for MS Isolation and Seismic Ruggedness (Unit 3), Rev. A
: BFN-50-7001, General Design Criteria for Main Steam System, Rev. 23 DCN T41019, Mods for MS Isolation and Seismic Ruggedness (Unit 3), Rev. A
: NEDC-31858P-A, BWROG Report for Increasing MSIV Leakage Rate Limits and Elimination of Leakage Control Systems, August 1999
: NEDC-31858P-A, BWROG Report for Increasing MSIV Leakage Rate Limits and Elimination of Leakage Control Systems, August 1999  
: Unit 2 Technical Specifications Section 3.6.2.2, Suppression Pool Water Level Unit 2 Technical Specifications Section 3.3.3.2, Backup Control System
: Unit 2 Technical Specifications Section 3.6.2.2, Suppression Pool Water Level Unit 2 Technical Specifications Section 3.3.3.2, Backup Control System
: PER 169830, Compliance Instrument 1-LI-64-54B Out of Tolerance
: PER 169830, Compliance Instrument 1-LI-64-54B Out of Tolerance
Line 772: Line 912:
: PER 171208), Uncontrolled Coatings Exceed Design Limit
: PER 171208), Uncontrolled Coatings Exceed Design Limit
: GEH-NE-0000-0103-0409, Increased Unqualified Coatings Assessment for Browns Ferry MDQ099920060011, Transient NPSH/Containment Pressure Evaluation of RHR and CS Pumps  
: GEH-NE-0000-0103-0409, Increased Unqualified Coatings Assessment for Browns Ferry MDQ099920060011, Transient NPSH/Containment Pressure Evaluation of RHR and CS Pumps  
: UFSAR Section 5.2, Primary Containment System UFSAR Section 6.5.5, Potential Plugging of Emergency Core Cooling System Suction Strainers Attachment
: UFSAR Section 5.2, Primary Containment System UFSAR Section 6.5.5, Potential Plugging of Emergency Core Cooling System Suction Strainers  
: Attachment


==Section 1R18: Plant Modifications==
==Section 1R18: Plant Modifications==
Line 832: Line 973:
: MCI-0-000-PCK001, General Maintenance Instructions for Valve Packing, Rev.21
: MCI-0-000-PCK001, General Maintenance Instructions for Valve Packing, Rev.21
: MSI-0-000-PLG001, Installation of Freeze Seals, Rev.34  
: MSI-0-000-PLG001, Installation of Freeze Seals, Rev.34  
: OPL171.006, Licensed Certification Training for Control Rod Blade and Drive Mechanism, Rev. 5 Drawing 2-47E820-2, Flow Diagram Control Rod Drive Hydraulic System, Rev.14 FSAR Section 3.4, Reactivity Control Mechanical Design,
: OPL171.006, Licensed Certification Training for Control Rod Blade and Drive Mechanism, Rev.
: Drawing 2-47E820-2, Flow Diagram Control Rod Drive Hydraulic System, Rev.14 FSAR Section 3.4, Reactivity Control Mechanical Design,
: BFN-22
: BFN-22
: WO 09-711929-000, North Header Supply to Core Spray II Cooler Valve Replacement
: WO 09-711929-000, North Header Supply to Core Spray II Cooler Valve Replacement
Line 841: Line 983:
: PER 170456,
: PER 170456,
: OI-67 Caused A3 EECW Pump to Operate Below Minimum Flow  
: OI-67 Caused A3 EECW Pump to Operate Below Minimum Flow  
: 1-SI-3.2.4, EECW Check Valve Test, Rev. 31 Tagout 0-TO-2009-0001, Clearance 0-067-0010, 1-SHV-067-0655
: 1-SI-3.2.4, EECW Check Valve Test, Rev. 31 Tagout 0-TO-2009-0001, Clearance 0-067-0010, 1-SHV-067-0655  
: Work Order 07-721562-002, Implement
: Work Order 07-721562-002, Implement
: DCN 69391, Stage 3 Work Order 07-721562-003, Uncouple and Couple 2D CS Pump from Motor Work Order 07-721562-005, Perform PMTs Following Replacement of 2D CS Pump Motor Work Order 07-721562-007, Perform Bridge and Megger on 2D CS Pump Motor 2-SR-3.5.1.6(CS
: DCN 69391, Stage 3 Work Order 07-721562-003, Uncouple and Couple 2D CS Pump from Motor Work Order 07-721562-005, Perform PMTs Following Replacement of 2D CS Pump Motor Work Order 07-721562-007, Perform Bridge and Megger on 2D CS Pump Motor 2-SR-3.5.1.6(CS
Line 879: Line 1,021:


==Section 1R20: Refueling and Other Outage Activities==
==Section 1R20: Refueling and Other Outage Activities==
: Browns Ferry Nuclear Plant Outage Risk Assessment Report Unit 2 Cycle 15 RFO Cycle 16, April 10, 2009 2-POI-200.5, Operations with Potential for Draining the Reactor Vessel/Cavity, Rev. 12 Drawing 2-47E820-2, Flow Diagram Control Rod Drive Hydraulic System, Rev. 14 2-AOI-100-1, Reactor Scram, Rev. 91 2-GOI-100-12A, Unit Shutdown from Power Operation to Cold Shutdown and Reductions in Power during Power Operations, Rev. 92 2-OI-1, Main Steam System, Rev. 45 2-GOI-100-3A, Refueling Operations (RX Vessel Disassembly and Floodup), Rev. 37 2-GOI-100-3B, Refueling Operations (Reactor Cavity Letdown and Vessel Re-Assembly), Rev. 48 2-SI-3.3.1.A, ASME Section XI System Leakage Test of the Reactor Vessel and Associated Piping, Rev. 25 2-SR-3.4.9.1(1), Reactor Heatup and Cooldown Rate Monitoring, Rev. 18 2-SR-3.3.2.1.2, RWM Functional Test for Startup, Rev. 3 2-SR-3.3.2.1.7, RWM Program Verification, Rev. 2 2-SR-3.1.3.5(A), Control Rod Coupling Integrity Check, Rev. 20  
: Browns Ferry Nuclear Plant Outage Risk Assessment Report Unit 2 Cycle 15 RFO Cycle 16, April 10, 2009 2-POI-200.5, Operations with Potential for Draining the Reactor Vessel/Cavity, Rev. 12 Drawing 2-47E820-2, Flow Diagram Control Rod Drive Hydraulic System, Rev. 14 2-AOI-100-1, Reactor Scram, Rev. 91 2-GOI-100-12A, Unit Shutdown from Power Operation to Cold Shutdown and Reductions in Power during Power Operations, Rev. 92 2-OI-1, Main Steam System, Rev. 45 2-GOI-100-3A, Refueling Operations (RX Vessel Disassembly and Floodup), Rev. 37 2-GOI-100-3B, Refueling Operations (Reactor Cavity Letdown and Vessel Re-Assembly), Rev.
: 2-SI-3.3.1.A, ASME Section XI System Leakage Test of the Reactor Vessel and Associated Piping, Rev. 25 2-SR-3.4.9.1(1), Reactor Heatup and Cooldown Rate Monitoring, Rev. 18 2-SR-3.3.2.1.2, RWM Functional Test for Startup, Rev. 3 2-SR-3.3.2.1.7, RWM Program Verification, Rev. 2 2-SR-3.1.3.5(A), Control Rod Coupling Integrity Check, Rev. 20  
: 2-SR-3.1.3.5(B), CRD Coupling Integrity Check After Refueling or Maintenance, Rev. 4
: 2-SR-3.1.3.5(B), CRD Coupling Integrity Check After Refueling or Maintenance, Rev. 4


==Section 1R22: Surveillance Testing==
==Section 1R22: Surveillance Testing==
: 1-SR-3.5.1.6(CS I), Quarterly CS System Flow Rate Test Loop I
: 1-SR-3.5.1.6(CS I), Quarterly CS System Flow Rate Test Loop I
: WO 08-724100-000, Electrical Maintenance PM for Monitoring CS Motor Bearing and Winding Temperatures BFN Unit 1 Technical Specifications Section 3.5.1, ECCS - Operating
: WO 08-724100-000, Electrical Maintenance PM for Monitoring CS Motor Bearing and Winding Temperatures BFN Unit 1 Technical Specifications Section 3.5.1, ECCS - Operating  
: 0-SR-3.8.1.9(D), Diesel Generator D Emergency Unit 2 Load Acceptance Test, Rev. 13 BFN Unit 1 Technical Specifications Section 3.8.1, AC Sources - Operating  
: 0-SR-3.8.1.9(D), Diesel Generator D Emergency Unit 2 Load Acceptance Test, Rev. 13 BFN Unit 1 Technical Specifications Section 3.8.1, AC Sources - Operating  
: BFN Unit 1 Technical Specifications Section 3.8.3, Diesel Generator Fuel Oil, Lube Oil and Starting Air BFN Unit 1 Technical Requirements Manual TRM 3.8.1, Diesel Generators BFN USFAR Section 8.5, Standby A-C Power Supply and Distribution
: BFN Unit 1 Technical Specifications Section 3.8.3, Diesel Generator Fuel Oil, Lube Oil and Starting Air BFN Unit 1 Technical Requirements Manual TRM 3.8.1, Diesel Generators BFN USFAR Section 8.5, Standby A-C Power Supply and Distribution  
: 2-SR-3.1.4.1, Scram Insertion Times, Rev. 26 Technical Specifications and Bases 3.1.4 Control Rod Scram Times, Amendment 295 Technical Specifications and Bases 3.1.3 Control Rod Operability, Amendment 253
: 2-SR-3.1.4.1, Scram Insertion Times, Rev. 26 Technical Specifications and Bases 3.1.4 Control Rod Scram Times, Amendment 295 Technical Specifications and Bases 3.1.3 Control Rod Operability, Amendment 253
: Attachment
: Attachment
: PER 174698, AUO Retrieved Valve Label from Radiological Contaminated Area with Bare Hands
: PER 174698, AUO Retrieved Valve Label from Radiological Contaminated Area with Bare Hands
: PER 175018,
: PER 175018,
: CRD 46-23 Declared Slow
: CRD 46-23 Declared Slow
: PER 175023, Evaluate Scram Insertion Time Testing on HWC Operation
: PER 175023, Evaluate Scram Insertion Time Testing on HWC Operation  
: 2-SR-3.4.3.2, Main Steam Relief Valve Manual Cycle Test
: 2-SR-3.4.3.2, Main Steam Relief Valve Manual Cycle Test
: BFN Unit 2 Technical Specifications Section 3.4.3, Safety/Relief Valves BFN Unit 2 Technical Specifications Bases Section 3.4.3, Safety/Relief Valves
: BFN Unit 2 Technical Specifications Section 3.4.3, Safety/Relief Valves BFN Unit 2 Technical Specifications Bases Section 3.4.3, Safety/Relief Valves
: PER 173480, MSRV 2-PCV-1-23 Failed to Fully Open During Manual Cycle Test
: PER 173480, MSRV 2-PCV-1-23 Failed to Fully Open During Manual Cycle Test
: PER 173480/WO 09-718047-000, Troubleshooting Plan
: PER 173480/WO 09-718047-000, Troubleshooting Plan  
: 2-SI-4.7.A.2.a-f, Primary Containment Integrated Leak Rate Test
: 2-SI-4.7.A.2.a-f, Primary Containment Integrated Leak Rate Test
: ANS 56.8 - 1994, Containment System Leakage Testing Requirements
: ANS 56.8 - 1994, Containment System Leakage Testing Requirements
Line 918: Line 1,061:
: RCI-33, Underwater Diving Operations, Rev. 7
: RCI-33, Underwater Diving Operations, Rev. 7
: RCI-40.3, RP Actions for Operation's Unit 3 Procedural Hold Points, Rev. 8
: RCI-40.3, RP Actions for Operation's Unit 3 Procedural Hold Points, Rev. 8
: RCI-41, Radiation Protection's Periodic Routines, Rev. 2
: RCI-41, Radiation Protection's Periodic Routines, Rev. 2  
: Records and Data Whole Body Count Results and Internal Dose Assessment, May 1-6, 2009  
: Records and Data Whole Body Count Results and Internal Dose Assessment, May 1-6, 2009  
: Dosimetry Investigation Report 08-093 Radiological Incident Reports:
: Dosimetry Investigation Report 08-093 Radiological Incident Reports:
: 20080044,
: 20080044,
: 20090011 SDE/DDE/LDE Calculation,
: 20090011 SDE/DDE/LDE Calculation,
: PC 20090011
: PC 20090011  
: Radiation Work Permits Attachment
: Radiation Work Permits
: Attachment
: 08330061, Unit 3 Maintenance on Heater Vents/Drains (Various Dress)
: 08330061, Unit 3 Maintenance on Heater Vents/Drains (Various Dress)
: 08372135, U3C13 Laundry/Trash Pickup/Labcoat Dressout
: 08372135, U3C13 Laundry/Trash Pickup/Labcoat Dressout
Line 933: Line 1,077:
: 280025, U2C15 Drywell Radcon Outage Support (Dose Control/High Rad/Various Dress)
: 280025, U2C15 Drywell Radcon Outage Support (Dose Control/High Rad/Various Dress)
: 09280095, U2C15 DW ISI, IWE, Fac (High Rad/Various Dress)
: 09280095, U2C15 DW ISI, IWE, Fac (High Rad/Various Dress)
: 09290018, U2C15 Refuel Floor Steam Dryer Tie Bar Repair (LHRA, Extremity & Multibadging)
: 09290018, U2C15 Refuel Floor Steam Dryer Tie Bar Repair (LHRA, Extremity & Multibadging)  
: Radiation Surveys
: Radiation Surveys
: 051209-32, Unit 2 Drywell 628'
: 051209-32, Unit 2 Drywell 628'
Line 993: Line 1,137:
: SPP-7.0, Work Management, Rev. 1
: SPP-7.0, Work Management, Rev. 1
: SPP-7.1, On Line Work Management, Rev. 12
: SPP-7.1, On Line Work Management, Rev. 12
: SPP-7.2, Outage Management, Rev. 12
: SPP-7.2, Outage Management, Rev. 12  
: Records and Data Reviewed
: Records and Data Reviewed Fiscal Year 2008 Annual ALARA Report Outage Report: BFN Unit 1 Cycle 8- February 2009 Forced Outage Declared Pregnant Women Dosimetry Documentation for 4 Women Browns Ferry Nuclear Power Plant Long-Term Collective Radiation Exposure Reduction Plan 2007 - 2011
: Fiscal Year 2008 Annual ALARA Report Outage Report: BFN Unit 1 Cycle 8- February 2009 Forced Outage Declared Pregnant Women Dosimetry Documentation for 4 Women Browns Ferry Nuclear Power Plant Long-Term Collective Radiation Exposure Reduction Plan 2007 - 2011
: APR 08-0005, Unit 1 Reactor Building 664' Elevation Refuel Floor, Rev.0
: APR 08-0005, Unit 1 Reactor Building 664' Elevation Refuel Floor, Rev.0
: APR 08-0107, U1C7 Outage - Modifications To Steam Dryer To Support EPU Conditions, Rev. 3
: APR 08-0107, U1C7 Outage - Modifications To Steam Dryer To Support EPU Conditions, Rev.
: APR 08-0110, U1C7 Outage - Scaffolding Support, Rev.0
: APR 08-0110, U1C7 Outage - Scaffolding Support, Rev.0
: APR 08-0111, U1C7 Outage - Insulation & Shielding - Remove, Maintain & Install, Rev. 0
: APR 08-0111, U1C7 Outage - Insulation & Shielding - Remove, Maintain & Install, Rev. 0
Line 1,018: Line 1,161:
: TSR 07-0037, Hot spots in the Unit 2 East and West Scram Discharge Volume Cages
: TSR 07-0037, Hot spots in the Unit 2 East and West Scram Discharge Volume Cages
: TSR 09-0002, U2C15 Outage Torus Snubber Bay 8 &11
: TSR 09-0002, U2C15 Outage Torus Snubber Bay 8 &11
: TSR 09-0003, Unit 2 Reactor Building 664' elevation, Refuel Floor, R-9 and S-Line South of the SFSP
: TSR 09-0003, Unit 2 Reactor Building 664' elevation, Refuel Floor, R-9 and S-Line South of the  
: SFSP
: TSR 09-0004, U2C15 Outage Drywell "Appendix A"
: TSR 09-0004, U2C15 Outage Drywell "Appendix A"
: TSR 09-0006, U2C15 Outage In-Vessel Inspection Platform
: TSR 09-0006, U2C15 Outage In-Vessel Inspection Platform
Line 1,035: Line 1,179:
: TSR 09-0025, U2C15 "D" MSIV in the U2 Steam Tunnel
: TSR 09-0025, U2C15 "D" MSIV in the U2 Steam Tunnel
: TSR 09-0034, U2C15 Junction of 3" and 4" Demin 2B Precoat Inlet Line (Photo attached)
: TSR 09-0034, U2C15 Junction of 3" and 4" Demin 2B Precoat Inlet Line (Photo attached)
: TSR 09-0048, U2C15 FPC Valves 2-DRV-078-559 & 560
: TSR 09-0048, U2C15 FPC Valves 2-DRV-078-559 & 560  
: CAP Documents Fiscal Year 2008 Annual ALARA Report Outage Report: BFN Unit 1 Cycle 8- February 2009 Forced Outage Browns Ferry Nuclear Power Plant Long-Term Collective Radiation Exposure Reduction Plan 2007 - 2011
: CAP Documents Fiscal Year 2008 Annual ALARA Report Outage Report: BFN Unit 1 Cycle 8- February 2009 Forced Outage Browns Ferry Nuclear Power Plant Long-Term Collective Radiation Exposure Reduction Plan 2007 - 2011
: PER 153752 Documenting Source Term Reduction Efforts Being Deferred
: PER 153752 Documenting Source Term Reduction Efforts Being Deferred
Line 1,052: Line 1,196:


==Section 2PS2: Radioactive Material Processing and Transportation==
==Section 2PS2: Radioactive Material Processing and Transportation==
: Procedures, Manuals, and Guides 0-OI-77A, Waste Collector/Surge System Processing, Rev. 57  
: Procedures, Manuals, and Guides
: 0-OI-77A, Waste Collector/Surge System Processing, Rev. 57  
: 0-OI-77B, Floor Drain Collector System Processing, Rev. 57 0-OI-77C, Radwaste Filter and Demineralizer System, Rev. 39
: 0-OI-77B, Floor Drain Collector System Processing, Rev. 57 0-OI-77C, Radwaste Filter and Demineralizer System, Rev. 39
: 0-OI-77D, Backwash Receivers and Phase Separators System, Rev. 34 0-OI-77E, Solid Radwaste, Rev. 41 0-OI-77F, Thermex Operation, Rev. 20 0-OI-77G, Duratek Procedure
: 0-OI-77D, Backwash Receivers and Phase Separators System, Rev. 34 0-OI-77E, Solid Radwaste, Rev. 41 0-OI-77F, Thermex Operation, Rev. 20 0-OI-77G, Duratek Procedure
Line 1,067: Line 1,212:
: RWTP-102, Use of Casks, Rev. 1  
: RWTP-102, Use of Casks, Rev. 1  
: SPP 3.1, Corrective Action Program, Rev. 15
: SPP 3.1, Corrective Action Program, Rev. 15
: SPP-5.1, Radiological Controls, Rev. 6
: SPP-5.1, Radiological Controls, Rev. 6  
: Shipping Records and Radwaste Data 10 CFR Part 61 Reports of Analysis/Certificates of Conformance, 09/28/07 and 02/02/09  
: Shipping Records and Radwaste Data
: CFR Part 61 Reports of Analysis/Certificates of Conformance, 09/28/07 and 02/02/09  
: Browns Ferry Nuclear Plant (BFN) - Personnel Qualified to Ship Radioactive Material/Waste Letter to File, March 3, 2009 BFN - Units 1, 2, and 3 - Annual Radioactive Effluent Release (ARER) Reports - January through December for 2007 and 2008 Cask Book for Model CNS 8-120B, Rev. 30 Safety Analysis Report 14-195H Shipping Cask, Rev. 2 Shipment No.
: Browns Ferry Nuclear Plant (BFN) - Personnel Qualified to Ship Radioactive Material/Waste Letter to File, March 3, 2009 BFN - Units 1, 2, and 3 - Annual Radioactive Effluent Release (ARER) Reports - January through December for 2007 and 2008 Cask Book for Model CNS 8-120B, Rev. 30 Safety Analysis Report 14-195H Shipping Cask, Rev. 2 Shipment No.
: 080106, Cask of Dewatered Resin, 01/17/08  
: 080106, Cask of Dewatered Resin, 01/17/08  
Line 1,081: Line 1,227:
: 090519, Sealand of Plant Waste, 05/20/09 Shipment No.
: 090519, Sealand of Plant Waste, 05/20/09 Shipment No.
: 090520, Sealand of Plant Waste, 05/20/09 Shipment No.
: 090520, Sealand of Plant Waste, 05/20/09 Shipment No.
: 090521, Sealand of Contaminated Plant Protective Clothing, 05/20/09
: 090521, Sealand of Contaminated Plant Protective Clothing, 05/20/09  
: CAP Documents
: CAP Documents
: PER 138682, Yellow radioactive material trash was inadvertently loaded and positioned near the bottom of a Sealand with contact dose rate reading of 400 mr/hr
: PER 138682, Yellow radioactive material trash was inadvertently loaded and positioned near the bottom of a Sealand with contact dose rate reading of 400 mr/hr
Line 1,091: Line 1,237:
==Section 4OA1: Performance Indicator Verification==
==Section 4OA1: Performance Indicator Verification==
: Browns Ferry Units 1/2/3 Mitigating Systems Performance Indicator MS05 through Q1/2009
: Browns Ferry Units 1/2/3 Mitigating Systems Performance Indicator MS05 through Q1/2009
: SPP-3.4, Performance Indicator and MOR Submittal Using INPO Consolidated Data Entry, Rev. 7
: SPP-3.4, Performance Indicator and MOR Submittal Using INPO Consolidated Data Entry, Rev.
: NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Rev. 5 NUREG 1022, Event Reporting Guidelines 10CFR 50.72 and 50.73, Rev. 2
: NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Rev. 5 NUREG 1022, Event Reporting Guidelines 10CFR 50.72 and 50.73, Rev. 2
: LER 05000296/2007-004, Manual Isolation of High Pressure Core Injection due to Steam Leak
: LER 05000296/2007-004, Manual Isolation of High Pressure Core Injection due to Steam Leak
Line 1,104: Line 1,250:
: O-SI-4.8.A.5-1, Appendix I Dose Calculations-Liquid Effluents
: O-SI-4.8.A.5-1, Appendix I Dose Calculations-Liquid Effluents
: CI-138, Reporting NEI Indicators  
: CI-138, Reporting NEI Indicators  
: O-SI-4.8.B.3, Appendix I Dose Calculations - Airborne Effluents Radiological Impact Assessment Report, January 2008-December 2008 Select Dosimetry Incident Reports involving dose rate alarms exceeding 1 rem/hr Semi-Annual Radioactive Effluent Release Report 2 (1st Quarter 2009)
: O-SI-4.8.B.3, Appendix I Dose Calculations - Airborne Effluents Radiological Impact Assessment Report, January 2008-December 2008 Select Dosimetry Incident Reports involving dose rate alarms exceeding 1 rem/hr Semi-Annual Radioactive Effluent Release Report 2 (1
st Quarter 2009)
: Batch Liquid Effluent Permit (March 14, 2009)
: Batch Liquid Effluent Permit (March 14, 2009)
: Gaseous Radioactive Waste Release Permit (March 18, 2009)
: Gaseous Radioactive Waste Release Permit (March 18, 2009)
Line 1,148: Line 1,295:
: [[CAP]] [[corrective action program]]
: [[CAP]] [[corrective action program]]
: [[CCW]] [[condenser circulating water]]
: [[CCW]] [[condenser circulating water]]
: [[CFR]] [[Code of Federal Regulations CoC  certificate of compliance]]
CFR Code of Federal Regulations
CoC  certificate of compliance
: [[CRD]] [[control rod drive]]
: [[CRD]] [[control rod drive]]
: [[CS]] [[core spray DCN design change notice]]
: [[CS]] [[core spray]]
: [[DCN]] [[design change notice]]
: [[EECW]] [[emergency equipment cooling water]]
: [[EECW]] [[emergency equipment cooling water]]
: [[EDG]] [[emergency diesel generator FE functional evaluation]]
: [[EDG]] [[emergency diesel generator]]
: [[FE]] [[functional evaluation]]
: [[FPR]] [[Fire Protection Report]]
: [[FPR]] [[Fire Protection Report]]
: [[FSAR]] [[Final Safety Analysis Report]]
: [[FSAR]] [[Final Safety Analysis Report]]
: [[IMC]] [[Inspection Manual Chapter]]
: [[IMC]] [[Inspection Manual Chapter]]
: [[LER]] [[licensee event report NCV non-cited violation]]
: [[LER]] [[licensee event report]]
: [[NRC]] [[U.S. Nuclear Regulatory Commission]]
: [[NCV]] [[non-cited violation]]
: [[ODCM]] [[Off-Site Dose Calculation Manual PER problem evaluation report]]
: [[NRC]] [[]]
: [[U.S.]] [[Nuclear Regulatory Commission]]
: [[ODCM]] [[Off-Site Dose Calculation Manual]]
: [[PER]] [[problem evaluation report]]
: [[PCIV]] [[primary containment isolation valve]]
: [[PCIV]] [[primary containment isolation valve]]
: [[PI]] [[performance indicator]]
: [[PI]] [[performance indicator]]
Line 1,166: Line 1,319:
: [[RHR]] [[residual heat removal]]
: [[RHR]] [[residual heat removal]]
: [[RHRSW]] [[residual heat removal service water]]
: [[RHRSW]] [[residual heat removal service water]]
: [[RTP]] [[rated thermal power RPS reactor protection system]]
: [[RTP]] [[rated thermal power]]
: [[RPS]] [[reactor protection system]]
: [[RWP]] [[radiation work permit]]
: [[RWP]] [[radiation work permit]]
: [[SDP]] [[significance determination process]]
: [[SDP]] [[significance determination process]]
: [[SB]] [[]]
: [[SBGT]] [[standby gas treatment]]
: [[GT]] [[standby gas treatment]]
: [[SLC]] [[standby liquid control]]
: [[SLC]] [[standby liquid control]]
: [[SNM]] [[special nuclear material SRV safety relief valve]]
: [[SNM]] [[special nuclear material]]
: [[SRV]] [[safety relief valve]]
: [[SSC]] [[structure, system, or component]]
: [[SSC]] [[structure, system, or component]]
: [[TI]] [[Temporary Instruction TIP transverse in-core probe]]
: [[TI]] [[Temporary Instruction]]
: [[TIP]] [[transverse in-core probe]]
: [[TRM]] [[Technical Requirements Manual]]
: [[TRM]] [[Technical Requirements Manual]]
: [[TS]] [[Technical Specification(s)]]
: [[TS]] [[Technical Specification(s)]]
: [[UFS]] [[]]
: [[UFSAR]] [[Updated Final Safety Analysis Report]]
: [[AR]] [[Updated Final Safety Analysis Report]]
: [[URI]] [[unresolved item]]
: [[URI]] [[unresolved item]]
: [[WO]] [[work order]]
: [[WO]] [[work order]]
}}
}}

Revision as of 19:36, 25 August 2018

IR 05000259-09-003, 05000260-09-003 and 05000296-09-003, on 04/01/2009 - 06/30/2009, Browns Ferry Nuclear Plant, Units 1, 2 and 3, Maintenance Risk Assessment, Access Control to Radiologically Significant Areas, and Event Followup
ML092120168
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 07/30/2009
From: Guthrie E F
Reactor Projects Region 2 Branch 6
To: Swafford P D
Tennessee Valley Authority
References
FOIA/PA-2010-0209 IR-09-003
Download: ML092120168 (60)


Text

July 30, 2009

Mr. Preston Chief Nuclear Officer and Executive Vice President Tennessee Valley Authority 3R Lookout Place 1101 Market Street Chattanooga, TN 37402-2801

SUBJECT: BROWNS FERRY NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT 05000259/2009003, 05000260/2009003 AND 05000296/2009003

Dear Mr. Swafford:

On June 30, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Browns Ferry Nuclear Plant, Units 1, 2, and 3. The enclosed inspection report documents the inspection results which were discussed, on July 6 and 17, 2009, with Mr. James Randich and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

In addition to the routine Reactor Oversight Process baseline inspections for all three units, the inspectors continued to conduct augmented inspections on Unit 1, as required, in accordance with NRC letters dated May 16, 2007, December 6, 2007, and May 21, 2008. These Unit 1 augmented inspections were conducted to compensate for the lack of valid data for the Mitigating Systems Performance Index (MSPI) Performance Indicators (PIs). The augmented inspections are only considered to be an interim substitute for the invalid Unit 1 MSPI PIs until such time as complete and accurate PI data is developed and declared valid.

Based on the results of this inspection, one NRC-identified finding and three self-revealing findings of very low safety significance (Green) were identified. Three of these findings were determined to involve violations of NRC requirements. Additionally, a licensee-identified violation which was determined to be of very low safety significance is listed in this report. However, because of their very low safety significance and because they were entered into your corrective action program, the NRC is treating these findings as non-cited violations (NCV(s)) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Senior Resident Inspector at Browns Ferry Nuclear Plant.

TVA 2 In addition, if you disagree with the characterization of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at Browns Ferry Nuclear Plant. The information you provide will be considered in accordance with Inspection Manual Chapter 0305.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response, if any, will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA/

Eugene F. Guthrie, Chief Reactor Projects Branch 6 Division of Reactor Projects Docket Nos.: 50-259, 50-260, 50-296 License Nos.: DPR-33, DPR-52, DPR-68

Enclosure:

Inspection Report 05000259/2009003, 05000260/2009003 and 05000296/2009003

w/Attachment:

Supplemental Information

cc w/encl. (See page 3)

_________________________ X SUNSI REVIEW COMPLETE OFFICE RII:DRP RII:DRP RII:DRP RII:DRP RII:DRS RII:DRS RII:DRS RII:DRS RII:DRP SIGNATURE PH TR by fax By email KK by emailRW by email BB for BB for BB for EG NAME PHiggins TRoss CStancil KKorth RWilliams HGepford RHamilton WLoo EGuthrie DATE 07/30/2009 07/30/2009 7/31/2009 07/30/2009 07/30/2009 7/31/2009 7/31/2009 7/31/2009 07/30/2009 E-MAIL COPY? YES/NO YES/NO YES/NO YES/NO YES/NO YES/NO YES/NO YES/NO YES/NO TVA 3 cc w/encl: Ashok S. Bhatnagar Senior Vice President Nuclear Generation Development and Construction 6A Lookout Place 1101 Market Street Chattanooga, TN 37402-2801 Preston Chief Nuclear Officer and Executive Vice President Tennessee Valley Authority 3R Lookout Place 1101 Market Street Chattanooga, TN 37402-2801 William R. Campbell Senior Vice President, Fleet Engineering Tennessee Valley Authority 6A Lookout Place 1101 Market Street Chattanooga, Tennessee 37402-2801

Tom Coutu Vice President Nuclear Support Tennessee Valley Authority 3R Lookout Place 1101 Market Street Chattanooga, TN 37402-2801 R. G. (Rusty) West Site Vice President Browns Ferry Nuclear Plant Tennessee Valley Authority Electronic Mail Distribution

Frederick Russell Godwin Manager, Licensing & Industry Affairs Browns Ferry Nuclear Plant Tennessee Valley Authority Electronic Mail Distribution James J. Randich Plant Manager Browns Ferry Nuclear Plant Tennessee Valley Authority Electronic Mail Distribution

General Counsel Tennessee Valley Authority 6A West Tower 400 West Summit Hill Drive Knoxville, TN 37902

Larry E. Nicholson General Manager Performance & Performance Improvement Tennessee Valley Authority Electronic Mail Distribution Michael A. Purcell Senior Licensing Manager Nuclear Power Group Tennessee Valley Authority Electronic Mail Distribution

Michael J. Lorek Interim Vice President Nuclear Engineering and Projects Tennessee Valley Authority Electronic Mail Distribution Fredrick C. Mashburn Acting Manager, Corporate Nuclear Licensing & Industry Affairs Tennessee Valley Authority Electronic Mail Distribution Mr. Robert J. Whalen Vice President, Nuclear Engineering Tennessee Valley Authority 3R Lookout Place 1101 Market Street Chattanooga, Tennessee 37402-2801

State Health Officer Alabama Dept. of Public Health RSA Tower - Administration Suite 1552 P.O. Box 303017 Montgomery, AL 36130-3017

Chairman Limestone County Commission 310 West Washington Street Athens, AL 35611 TVA 4 Letter to Preston from Eugene F. Guthrie dated July 30, 2009

SUBJECT: BROWNS FERRY NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT 05000259/2009003, 05000260/2009003 AND 05000296/2009003 Distribution w/encl:

E. Brown, NRR L. Raghavan, NRR C. Evans, RII L. Slack, RII T. Ross, SRI Browns Ferry OE Mail RIDSNRRDIRS PUBLIC Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION II

Docket Nos.: 50-259, 50-260, 50-296

License Nos.: DPR-33, DPR-52, DPR-68

Report No.: 05000259/2009003, 05000260/2009003 and 05000296/2009003 Licensee: Tennessee Valley Authority (TVA)

Facility: Browns Ferry Nuclear Plant, Units 1, 2, and 3

Location: Corner of Shaw and Nuclear Plant Roads Athens, AL 35611

Dates: April 1, 2009 through June 30, 2009 Inspectors: T. Ross, Senior Resident Inspector C. Stancil, Resident Inspector K. Korth, Resident Inspector R. Williams, Reactor Inspector (1R08) H. Gepford, Senior Health Physicist (2OS1, 2PS1, 4OA1, 4OA7) R. Hamilton, Senior Health Physicist (2OS2)

W. Loo, Senior Health Physicist (2PS2)

Approved by: Eugene F. Guthrie, Chief Reactor Projects Branch 6 Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000259/2009003, 05000260/2009003 and 05000296/2009003; 04/01/2009 - 06/30/2009; Browns Ferry Nuclear Plant, Units 1, 2 and 3;

Maintenance Risk Assessment, Access Control to Radiologically Significant Areas, and Event Followup.

The report covered a three month period of inspection by resident inspectors and reactor inspectors from the region

. Three non-cited violations (NCV) and one Finding (FIN) were identified. The significance of most findings is identified by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process" Revision 4, dated December 2006.

A. NRC Identified and Self-Revealing Findings

Cornerstone: Initiating Events

Green.

A Green self-revealing finding was identified for a failure to implement corrective actions in a timely manner to address excessive isophase bus cooling (IBC) system condensation that resulted in a main generator trip and Unit 1 reactor scram caused by water accumulation in the IBC ductwork, which created an electrical ground fault on the main generator isophase busses. An additional drain line was subsequently installed, and operating procedures were revised, to ensure any excessive condensation buildup would be removed from the IBC system during winter operation. This event was entered into the licensee's corrective action program as PER 163815.

This finding was determined to be greater than minor because it was associated with the Initiating Event Cornerstone attribute of Equipment Performance, and adversely affected the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during at-power operations. The finding was evaluated using Phase 1 of the At-Power Significance Determination Process, and was determined to be of very low safety significance (Green) because it did not contribute to both the likelihood of a reactor trip and the likelihood that mitigating equipment or functions were not available. The cause of this finding was directly related to the cross-cutting aspect of appropriate and timely corrective actions in the area of Problem Identification and Resolution because the license had identified an abnormal equipment condition related to excessive IBC system condensation for which specified corrective actions were not carried out (P.1.d). (Section 4OA3.2)

Cornerstone: Mitigating Systems

Green.

A Green self-revealing noncited violation of 10 CFR Part 50.65 (a)(4), "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants," was identified for failure to adequately assess and manage shutdown risk associated with maintenance activities. Specifically, on May 2, 2009, the licensee performed a scheduled activity to install the 2A Recirculation Line nozzle plug in the reactor vessel. Installation of this plug isolated the common residual heat removal (RHR) system shutdown cooling (SDC) suction path while SDC availability was assumed in the shutdown risk assessment and had been designated as protected equipment as part of the specified risk management actions. Shortly after the nozzle plug was installed, the licensee recognized that SDC was no longer immediately available and promptly removed the plug to restore SDC availability. This event was entered into the licensee's corrective action program as problem evaluation report 170184. This finding affected the Mitigating Systems cornerstone and was determined to be greater than minor because the licensee failed to effectively manage the prescribed significant compensatory measures (i.e., protection of Loop I RHR). The significance of this finding was evaluated using Inspection Manual Chapter (IMC 0609), Appendix G, "Shutdown Operations Significance Determination Process," Table 1, "Losses of Control," and Checklist 7 of Attachment 1, "BWR Refueling Operation with RCS Level > 23' ", the inspectors determined that this finding was of very low safety significance (Green) because the event did not result a loss of control per Table 1 of Appendix G, or an actual loss of decay heat removal, and the SDC alignment was restored well within the time to boil. The cause of this finding was directly related to the cross cutting aspect of work activity coordination in the area of Human Performance, because the licensee failed to adequately evaluate the impact of the work and to communicate, coordinate, and cooperate with each other during activities in which interdepartmental coordination is necessary to assure plant performance (H.3.b). (Section 1R13).

Green.

A Green non-cited violation of 10 CFR Part 50.65 (a)(4), "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants," was identified when the licensee failed to consider the impact of severe weather conditions on plant risk. Specifically, on May 1 and again on May 2, 2009, the licensee removed the A Emergency Diesel from service for planned maintenance during severe weather conditions (i.e., Tornado Warning and Tornado Watch, respectively) without re-evaluating the potential adverse affect upon the existing on-line risk assessment. The severe weather conditions only lasted about an hour each day. This issue was entered into the licensee's corrective action program as problem evaluation report 171402. The finding was determined to be greater than minor because the licensee's risk assessment failed to consider unusual external conditions that were present or imminent (e.g., severe weather, offsite power instability). According to Inspection Manual Chapter 0609, Appendix K, Maintenance Risk Assessment and Risk Management Significance Determination Process, the significance of this finding was determined to be of very low safety significance (Green) based on an initiating events frequency of <1.0E-7, and a very low risk deficit due to the number of redundant emergency diesels and the short duration of the severe weather. The cause of this finding was directly related to the crosscutting aspect of complete and accurate procedures in the area of Human Performance because the licensee's site-specific guidelines for assessing on-line risk did not require severe weather to be considered when determining plant risk nor did they require personnel to determine if severe weather is imminent prior to removing an emergency diesel generator from service (H.2.c). (Section 1R13).

Cornerstone: Occupational Radiation Safety

  • Green A Green self-revealing non-cited violation of Technical Specifications 5.4.1, Procedures, was identified for a radiation worker who failed to follow the requirements of Radiation Work Permit 09270081 as required by procedure RCI-9.1, Radiation Work Permits, Rev. 57. The licensee has entered this issue into the corrective action program as problem evaluation report 171375. This finding is greater than minor because it is associated with the Occupational Radiation Safety Cornerstone attribute of Program and Process (Exposure Control) and adversely affected the cornerstone objective of ensuring adequate protection of worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation. The finding was evaluated using the Occupational Radiation Safety Significance Determination Process and determined to be of very low safety significance (Green) because it was not related to As Low As Reasonably Achievable (ALARA) planning, nor did it involve an overexposure or substantial potential for overexposure, and the ability to assess dose was not compromised. The cause of this finding was directly related to the cross-cutting aspect of work practices in the area of Human Performance, because the radiation worker failed to use self-checking prior to passing through the swing gate into the posted high radiation area (H.4.a). (Section 2OS1)

B. Licensee Identified Violations

One violation of very low safety significance, which was identified by the licensee, has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. This violation and the corrective action program tracking number are listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

Unit 1 operated at full rated thermal power (RTP) the entire report period except for three planned downpowers. On May 2, 2009, a planned downpower to approximately 90 percent RTP was conducted to perform a control rod adjustment. The unit was returned to full RTP the same day. On June 6, 2009, a planned downpower to approximately 70 percent RTP was conducted to execute a control rod sequence exchange. The unit was returned to full RTP the same day. On June 12, 2009, a planned downpower to approximately 75 percent RTP was conducted to repair Main Turbine Generator #3 Control Valve. The unit was returned to full RTP the same day.

Unit 2 began this report period at full RTP.

On April 11, 2009, a planned downpower to 80 percent RTP was conducted to execute a control rod adjustment. The unit returned to full RTP on the same day. On April 25, 2009, the unit was shutdown for the Unit 2 Cycle 15 (U2C15) refueling outage. The unit was restarted June 8, 2009, but had to shutdown from approximately 15 percent RTP due to a sudden increase in unidentified reactor coolant system (RCS) leakage in excess of the Technical Specification limit of 2 gallons per minute in the previous 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Following repairs, the reactor was restarted on June 15, 2009. The unit was shutdown again from approximately 14 percent RTP on June 16, 2009 due to failure of the same MSRV to properly lift and reseat during testing. After the MSRV was replaced, Unit 2 was restarted on June 20, 2009. The unit achieved full RTP power on June 27, 2009 and remained at full RTP for the remainder of the report period.

Unit 3 operated at full RTP the entire report period except for eight planned downpowers. Four of the power reductions were conducted to between 90 and 95 percent RTP to repair reactor feedwater heater or moisture separator normal level control valves. These downpowers were conducted on April 3, May 22, May 29, and June 23, 2009, and in each case, power was restored to full RTP on the same day. On April 4, 2009, a downpower was conducted to 75 percent RTP for a control rod adjustment. On April 15, 2009, a downpower to approximately 58 percent RTP was conducted to replace two power cells in the 3B Variable Frequency Drive.

The unit was returned to full RTP on April 17, 2009. On May 21, 2009, a planned downpower to approximately 95 percent RTP was conducted to recover a control rod that had been inserted for maintenance, and promptly returned to full RTP. Then on June 27, power was reduced to 75 percent for a rod sequence exchange and main condenser cleaning. The unit was returned to full RTP the same day.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R01 Adverse Weather Protection

.1 Readiness for Seasonal Extreme Weather Conditions

a. Inspection Scope

Prior to and during the onset of hot weather conditions, the inspectors reviewed the licensee's implementation of 0-GOI-200-3, Hot Weather Inspection, including 6 Enclosure Attachment 1, Hot Weather Operational Checklist. The inspectors also reviewed the Hot Weather Discrepancy Log (PA-104); and discussed implementation of 0-GOI-200-3 with responsible Work Control and Operations personnel and management. Furthermore, the inspectors conducted walkdowns of potentially affected risk significant equipment systems relied on to cool the 480v and 4Kv Shutdown Board Rooms.

b. Findings

No findings of significance were identified.

.2 Offsite and Alternate AC Power Systems Readiness

a. Inspection Scope

Prior to the summer season, inspectors reviewed electrical power design features, onsite risk and work management procedures, and corporate transmission and power supply procedures to verify appropriate operational oversight and assurance of continued availability of offsite and alternate AC power systems. Inspectors verified that communications protocols existed between the transmission system operator and Browns Ferry Nuclear Plant for coordination of off-normal and emergency events affecting the plant, event details, estimates of return-to-service times, and notifications of grid status changes. Inspectors also verified that procedures included controls to adequately monitor both offsite AC power systems (including post-trip voltages) and onsite alternate AC power systems for availability and reliability. Furthermore, inspectors interviewed onsite licensed operators and offsite transmission personnel to determine their understanding and implementation of the power monitoring and assessment process. Inspectors reviewed the material condition of offsite AC power systems and onsite alternate AC power systems to the plant, including switchyard and transformers. This review included review of outstanding work orders affecting these systems and a walkdown of the switchyard with operations personnel to ensure the systems will continue to provide appropriate "as designed" capabilities.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

.1 Partial Walkdown

a. Inspection Scope

The inspectors conducted three equipment partial alignment walkdowns to evaluate the operability of selected redundant trains or backup systems, listed below, with the other train or system inoperable or out of service. The inspectors reviewed the functional systems descriptions, Updated Final Safety Analysis Report (UFSAR), system operating procedures, and Technical Specifications (TS) to determine correct system lineups for the current plant conditions. The inspectors performed walkdowns of the systems to verify that critical components were properly aligned and to identify any discrepancies which could affect operability of the redundant train or backup system.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

.1 Routine Walkdowns

a. Inspection Scope

The inspectors reviewed licensee procedures, Standard Programs and Processes (SPP)-10.10, Control of Transient Combustibles, and SPP-10.9, Control of Fire Protection Impairments, and conducted a walkdown of the seven fire areas (FA) and fire zones (FZ) listed below. Selected FAs/FZs were examined in order to verify licensee control of transient combustibles and ignition sources; the material condition of fire protection equipment and fire barriers; and operational lineup and operational condition of fire protection features or measures. Also, the inspectors verified that selected fire protection impairments were identified and controlled in accordance with procedure SPP-10.9. Furthermore, the inspectors reviewed applicable portions of the Site Fire Hazards Analysis Volumes 1 and 2 and Pre-Fire Plan drawings to verify that the necessary fire fighting equipment, such as fire extinguishers, hose stations, ladders, and communications equipment, was in place.

  • Unit 1 Reactor Building Elev. 621, 1A Electrical Board Room (EBR) (FA-5)
  • Unit 1 Reactor Building Elev. 621, Shutdown Board Room 1A (FA-6)
  • Unit 1 Reactor Building Elev. 621, Shutdown Board Room 1B (FA-7)
  • Unit 2 Control Building Elev. 593, Battery Board Room 2 and Battery Room 2 (FA-18)
  • Unit 2 Reactor Building Elev. 639 South of Column Line R (FZ 2-6)
  • Unit 3 Reactor Building Elev. 593, 480v RMOV Board Room 3B (FA-12)
  • Unit 3 Reactor Building Elevs. 621 and 639 North of Column Line R (FZ 3-4)

b. Findings

No findings of significance were identified.

1R08 Inservice Inspection (ISI) Activities

.1 Non-Destructive Examination (NDE) Activities and Welding Activities

a. Inspection Scope

From May 4 to May 8, 2009, the inspectors observed and reviewed the implementation of the licensee's In-service Inspection (ISI) program for monitoring degradation of the reactor coolant system (RCS) boundary and risk significant piping boundaries. The inspectors' activities consisted of an on-site review of nondestructive examination (NDE)8 Enclosure and welding activities to evaluate compliance with the applicable edition of the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (BPVC),Section XI (Code of record: 1995 Edition with 1996 Addenda), and to verify that indications and defects (if present) were appropriately evaluated and dispositioned in accordance with the requirements of the ASME Code,Section XI acceptance standards. For Browns Ferry Unit 2, this was the first outage of the third period of the third interval.

The inspectors also reviewed a sample of inspection activities associated with components that are outside the scope of ASME Section XI requirements which are performed in accordance with commitments to follow industry guidance documents, such as the Boiling Water Reactor Vessel and Internals Project (BWRVIP).

The inspectors' review of NDE activities specifically covered examination procedures, NDE reports, equipment and consumables certification records, personnel qualification records, and calibration reports (as applicable) for the following examinations:

  • Phased array ultrasonic testing (UT) examination of weld GFW-2-32, ASME Class 1 Category B-J, Tee to pipe weld The inspectors reviewed the following examination from the previous outage with a relevant indication that was analytically evaluated and accepted for continued service to verify that the acceptance was in accordance with ASME Code:
  • NOI #U2C14-049 - N9 nozzle to vessel weld The inspectors' review of welding activities specifically covered the welding activity listed below in order to evaluate compliance with procedures and the ASME Code. The inspector reviewed the work order, repair and replacement plan, weld data sheets, welding procedures, procedure qualification records, welder qualification records, and NDE reports.
  • Welding package for work order #09-711929-000 - Welded replacement of valve BFR-1-SHV-067-0655

b. Findings

No findings of significance were identified.

.2 Reactor Vessel Internal Inspections

a. Inspection Scope

The inspectors reviewed the following NDE activities associated with the inspection of reactor vessel internal components per the BWRVIP:

  • EVT-1 of Jet Pump restrainer assemblies including the set screws and wedge assemblies
  • VT-3 of feed water sparger pins

9 Enclosure The inspectors also reviewed activities related to the planned repair and modification of select jet pump restrainer assemblies. For some assemblies, larger-than-allowable gaps between the jet pumps and set screws were seen during the visual examinations. The inspectors verified that planned repairs were being completed in accordance with BWRVIP requirements.

b. Findings

No findings of significance were identified.

.3 Identification and Resolution of Problems

a. Inspection Scope

The inspectors performed a review of ISI-related problems that were identified by the licensee and entered into the corrective action program. The inspectors reviewed these corrective action documents to confirm that the licensee had appropriately described the scope of the problem and had initiated corrective actions. The review also included the licensee's consideration and assessment of operating experience events applicable to the plant. The inspectors performed this review to ensure compliance with 10CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requirements. The corrective action documents reviewed by the inspectors are listed in the report attachment.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification

.1 Resident Inspector Quarterly Review

a. Inspection Scope

On April 6, 2009, the inspectors observed licensed operator requalification simulator examination for two crews. Each crew received the same examination scenario - "Group 6 Isolation and Main Steam Line Break in Containment".

The inspectors specifically evaluated the following attributes related to each operating crew's performance:

  • Clarity and formality of communication
  • Ability to take timely action to safely control the unit
  • Prioritization, interpretation, and verification of alarms
  • Correct use and implementation of Abnormal Operating Instructions (AOIs), and Emergency Operating Instructions (EOIs)
  • Timely and appropriate Emergency Action Level declarations per Emergency Plan Implementing Procedures (EPIP)
  • Control board operation and manipulation, including high-risk operator actions
  • Command and Control provided by the Unit Supervisor and Shift Manager 10 Enclosure The inspectors attended a post-examination critique to assess the effectiveness of the licensee evaluators, and to verify that licensee-identified issues were comparable to issues identified by the inspector. The inspectors also reviewed simulator physical fidelity (i.e., the degree of similarity between the simulator and the reference plant control room, such as physical location of panels, equipment, instruments, controls, labels, and related form and function).

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

.1 Routine

a. Inspection Scope

The inspectors reviewed two specific equipment issues listed below for structures, systems and components (SSC) within the scope of the Maintenance Rule (MR) pursuant to 10CFR50.65 with regard to some or all of the following attributes: (1) Work practices; (2) Identifying and addressing common cause failures; (3) Scoping in accordance with 10 CFR 50.65(b); (4) Characterizing reliability issues (e.g., functional failures); (5) Trending key parameters for condition monitoring; (6) Tracking SSC unavailability; (7) Appropriateness of performance criteria in accordance with 10 CFR 50.65(a)(2); (8) System classification in accordance with 10 CFR 50.65(a)(1); and (9) Appropriateness and adequacy of (a)(1) goals and corrective actions (i.e., Ten Point Plan). The inspectors also compared the licensee's performance against site procedure SPP-6.6, Maintenance Rule Performance Indicator Monitoring, Trending and Reporting; Technical Instruction 0-TI-346, Maintenance Rule Performance Indicator Monitoring, Trending and Reporting; and SPP 3.1, Corrective Action Program. The inspectors also reviewed, as applicable, work orders, surveillance records, problem evaluation reports (PERs), system health reports, engineering evaluations, and MR expert panel minutes; and attended MR expert panel meetings to verify that regulatory and procedural requirements were met.

  • Unit 2 HPCI System Unavailability Exceeded MR Performance Criteria.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Evaluation

a. Inspection Scope

For planned online work and/or emergent work that affected the combinations of risk significant systems listed below, the inspectors reviewed six licensee maintenance risk assessments and actions taken to plan and control work activities to effectively manage and minimize risk. The inspectors verified that risk assessments and applicable risk 11 Enclosure management actions (RMA) were conducted as required by 10 CFR 50.65(a)(4) and applicable plant procedures such as SPP-7.0, Work Management; SPP-7.1, On-Line Work Management; 0-TI-367, BFN Equipment to Plant Risk Matrix; and BP-336, Risk Determination And Risk Management. The inspectors also evaluated the adequacy of the licensee's risk assessments and implementation of RMAs.

  • Unit 2 CS Loop I, 2A Control Rod Drive (CRD) Pump, A Control Bay Chiller, 1A EBR Air Handling Unit, and 2A Condenser Circulating Water (CCW) Pump out of service (OOS)

b. Findings

The inspectors identified two findings involving maintenance risk assessments, as documented below.

.1 Inadequate Shutdown Risk Assessment During Outage Maintenance

Introduction:

A self-revealing non-cited violation (NCV) of 10 CFR Part 50.65 (a)(4), "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants," was identified for failure to adequately assess and manage shutdown risk associated with outage maintenance activities. Specifically, on May 2, 2009, the licensee performed a scheduled activity to install the 2A Reactor Recirculation suction line nozzle plug in the reactor vessel. This plug isolated the common shutdown cooling (SDC) suction path while SDC was assumed to be available in the existing outage risk assessment and had been designated as protected equipment .

Description:

On May 1, 2009, Unit 2 was in a refueling outage in Mode 5 with greater than 23' of water above the fuel and a time-to-boil of approximately 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The B secondary side alternate decay heat removal (ADHR) pump was out of service for unplanned maintenance. In accordance with SPP 7.2, Outage Management, a shutdown risk assessment was conducted using Outage Risk Assessment Management (ORAM) software. In order to maintain the unit in a Yellow outage risk condition for the decay heat removal safety function, the Loop I RHR system for SDC was being protected (i.e., risk management action) as a redundant system for decay heat removal. The ADHR system was in service using the A secondary side pump, SDC was secured but still available.

As part of the outage schedule, the 2A Reactor Recirculation suction line was to be plugged to perform outage maintenance. The predecessor activity to the reactor 12 Enclosure recirculation suction line nozzle plug installation was to ensure SDC was out of service. This activity was incorrectly reported as complete when RHR pumps were secured, and SDC was placed in standby, at which point the outage control center (OCC) directed Maintenance to install the plug. Multiple personnel in different organizations knew that the plug was being installed. However, it was not recognized and/or communicated that this action would isolate both the reactor water cleanup (RWCU) and SDC suction path, and thereby make the designated protected equipment unavailable for use. Shortly after the nozzle plug was installed, at 0016 on May 2, 2009, the Unit 2 control room received a RWCU Recirculation Pump Flow Low alarm and operators responded per the Alarm Response Procedure (ARP). Attempts were made to raise the flow per the ARP and when there was no response the 2A RWCU pump was secured. At 0030, the Main Control Room (MCR) staff was informed that the 2A Recirculation Line suction plug had been installed. Control room personnel promptly recognized that installation of this plug had resulted in the RWCU low flow condition and had effectively isolated shutdown cooling. Maintenance personnel were immediately directed to remove the plug. The nozzle plug was reported to be removed from the recirculation line at 0620 on May 2, 2009.

Analysis:

The inspectors determined that the risk management actions put in place pursuant to 10 CFR 50.65(a)(4) for in progress outage maintenance activities were not effectively managed to prevent disabling the protected SDC system and constituted a performance deficiency. This finding affected the Mitigating Systems cornerstone and was determined to be greater than minor according to Inspection Manual Chapter (IMC)0612, Appendix B, Issue Screening, because the licensee failed to effectively manage the prescribed significant compensatory measures (i.e. protection of Loop I RHR). The significance of this finding was evaluated using IMC 0609, Appendix K, Maintenance Risk Assessment and Risk Management Significance Determination Process, which stated that if the finding involved maintenance activities during shutdown conditions, then the appropriate checklist reflecting the plant shutdown mode from IMC 0609, Appendix G, Attachment 1, should be checked to determine risk significance. According to IMC 0609, Appendix G, "Shutdown Operations Significance Determination Process," Table 1, "Losses of Control," and Checklist 7 of Attachment 1, "BWR Refueling Operation with RCS Level > 23'" , the inspectors determined that this finding was of very low safety significance (Green) because the event did not result a loss of control per Table 1 of MC0609, Appendix G, or an actual loss of decay heat removal and the SDC alignment was restored well within the time to boil. As such, Appendix G did not require the significance of the finding to be quantified by a Phase 2 or 3 analysis. During the event, ADHR was in service removing reactor decay heat, and there was adequate time to restore SDC to service (i.e., remove the plug) before boiling of the RCS would occur if ADHR were lost (i.e., time to boil about 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />). The RHR SDC function was restored in a relatively short period of time (approximately 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />). The cause of this finding was directly related to the cross cutting aspect of work activity coordination in the area of Human Performance, because the licensee failed to adequately evaluate the impact of the work and to communicate, coordinate, and cooperate with each other during activities in which interdepartmental coordination is necessary to assure plant performance. Specifically, the OCC authorized installation of the recirculation line plug even though the plant was relying on SDC availability as defense in depth for their shutdown risk assessment (H.3.b).

Enforcement:

10 CFR 50.65(a)(4) required, in part, that prior to performing maintenance activities, the licensee shall assess and manage the increase in risk that may result from 13 Enclosure the proposed maintenance activities. Contrary to this, on May 2, 2009, the licensee failed to adequately assess and manage shutdown risk associated with outage maintenance activities related to SDC availability to provide for the decay heat removal safety function. Because the finding was determined to be of very low safety significance and has been entered into the licensee's CAP as PER 170184, this violation is being treated as an NCV consistent with Section VI.A of the Enforcement Policy: NCV 05000260/2009003-01, "Failure to Assess and Manage Shutdown Risk Associated With Outage Maintenance Activities."

.2 Failure to Perform an Adequate Risk Assessment during Severe Weather Conditions

Introduction:

The inspectors identified a Green NCV of 10 CFR 50.65(a)(4) involving the licensee's failure to consider the impact of severe weather on plant risk.

Description:

At 1550, on May 1, 2009, with Unit 1 at 100 percent power, the licensee removed the A EDG from service for planned maintenance while the A3 EECW pump and the RHR crosstie were already OOS. At 1611, a Tornado Warning was issued by the National Weather Service. However, the licensee failed to re-evaluate their risk assessment prior to, or during the onset of, severe weather conditions to consider the potential impact of severe weather on plant risk. The Tornado Warning expired at 1715. Then on May 2, 2009, the A EDG was declared inoperable for surveillance testing at 1503. At 1510, a Tornado Watch was issued by the National Weather Service. The licensee aborted the diesel surveillance and restored it to service, but severe weather conditions were not considered in the risk assessment either before or afterwards.

Section 3.2.A, of Standards Programs and Processes (SPP) 7.1, On-Line Work Management, required that a risk assessment of scheduled on-line maintenance be performed prior to implementation, and emergent work was to be evaluated against the assessed scope. According to section 3.2.B.1.n of SPP 7.1, this risk assessment was required to include external event considerations involving the potential impacts of weather or other external conditions relative to the proposed maintenance evolution if these external impacts (e.g., weather, external flooding, grid reliability, and other external impacts) were imminent or have a high probability of occurring during the planned out of service duration. Furthermore, section 3.2.2 of SPP 7.1, required that the assessment of risk for scheduled activities be re-performed if there were significant changes in external conditions (e.g., weather or offsite power availability). The licensee's failure to consider severe weather conditions as part of their on-line risk assessments on May 1 and 2, 2009, were contrary to the provisions of SPP-7.1.

The sub-tier instructions used by the licensee for assessing on-line risk at Browns Ferry included BP-336, Risk Determination and Risk Management, and 0-TI-367, BFN Equipment to Plant Risk Matrix. These Browns Ferry site specific guidelines did not include consideration of severe weather impact on on-line risk.

Analysis:

The failure of the licensee to consider the impact of severe weather on plant risk was a performance deficiency which could have led to underestimating the risk of plant maintenance activities and/or failure to take actions to minimize that risk. This finding was determined to be greater than minor according to IMC 0612, Appendix B, Issue Screening, because the licensee's risk assessment failed to consider unusual external conditions that were present or imminent (e.g., severe weather, offsite power instability). The significance of this finding was determined to be of very low safety significance (Green) according to IMC 0609, Appendix K, Maintenance Risk Assessment 14 Enclosure and Risk Management Significance Determination Process, based on an initiating events frequency of <1.0E-7, and a very low risk deficit due to the number of redundant emergency diesels and the short duration of the severe weather. This issue was entered into the licensee's corrective action program as PER 171402.

The cause of this finding was directly related to the crosscutting aspect of complete and accurate procedures in the area of Human Performance because the licensee's site specific guidelines for assessing on-line risk did not require severe weather to be considered when determining plant risk nor did they require personnel to determine if severe weather is imminent prior to removing an emergency diesel generator from service (H.2.c).

Enforcement:

10 CFR 50.65 (a)(4), required in part, that before performing maintenance activities (including but not limited to surveillance, post-maintenance testing, and corrective and preventive maintenance), the licensee shall assess and manage the increase in risk that may result from the proposed maintenance activities. Contrary to this, on May 1 and 2, 2009, plant personnel failed to assess and manage risk for maintenance activities during unusual external conditions (i.e., severe weather).

Because this finding was determined to be of very safety risk significance (Green) and has been entered into the licensee's CAP as PER 171402, this violation is being treated as an NCV, consistent with Section VI.A of the Enforcement Policy: NCV 05000259/2009003-02, "Failure to Perform an Adequate Risk Assessment during Severe Weather Conditions."

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the five operability/functional evaluations listed below to verify technical adequacy and ensure that the licensee had adequately assessed TS operability. The inspectors also reviewed applicable sections of the UFSAR to verify that the system or component remained available to perform its intended function. In addition, where appropriate, the inspectors reviewed licensee procedures NEDP-22, Functional Evaluations and PIDP-3, Operability and Reportability Reviews of PERs, to ensure that the licensee's evaluation met procedure requirements. Furthermore, where applicable, inspectors examined the implementation of compensatory measures to verify that they achieved the intended purpose and that the measures were adequately controlled. The inspectors also reviewed PERs on a daily basis to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations.

  • Unit 2 Core Spray Room Cooler Low Flow/Differential Pressure (PER 167344)
  • Unit 1 Turning Gear Oil Pump Failure to Load Shed from 480V Board (PER 166870)
  • Unit 1 Narrow Range Suppression Pool Level Indicators in Divergence (PER 169830)

b. Findings

No findings of significance were identified.

1R18 Plant Modifications

.1 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed one temporary modification listed below to verify regulatory requirements were met, along with procedures such as 0-TI-405, Plant Modifications and Design Change Control; 0-TI-410, Design Change Control; and SPP-9.5, Temporary Alterations. The inspectors also reviewed existing licensee documentation against the UFSAR and TS to verify that the modification did not affect operability or availability of the affected system. Furthermore, the inspectors walked down the modification to ensure that it was installed in accordance with the modification documents and reviewed post-installation and removal testing to verify that the actual impact on permanent systems was adequately verified by the tests.

  • PER 168128, Vibration Instrumentation for Monitoring Unit 3 RHRSW HX Outlet Valve Vibrations

b. Findings

No findings of significance were identified.

.2 Permanent Plant Modifications

a. Inspection Scope

The inspectors reviewed the Design Change Notice (DCN) and completed work packages (WO 08-724013-018 and 08-724013-21) for DCN 69528, Replace ASCO Solenoid Valves with Similar AVCO Valves, including related documents and procedures. The inspectors reviewed licensee procedures 0-TI-405, Plant Modifications and Design Change Control, and SPP-9.3, Plant Modifications and Engineering Change Control, and observed part of the licensee

=s activities to implement this design change made while the unit was online. The inspectors reviewed the associated 10 CFR 50.59 screening against the system design bases documentation to verify that the modifications had not affected system operability/availability. The inspectors reviewed selected ongoing and completed work activities to verify that installation was consistent with the design control documents.

b. Findings

No findings of significance were identified.

1R19 Post Maintenance Testing

16 Enclosure

a. Inspection Scope

The inspectors reviewed the six post-maintenance tests (PMT) listed below to verify that procedures and test activities confirmed SSC operability and functional capability following maintenance. The inspectors reviewed the licensee's completed test procedures to ensure any of the SSC safety function(s) that may have been affected were adequately tested, that the acceptance criteria were consistent with information in the applicable licensing basis and/or design basis documents, and that the procedure had been properly reviewed and approved. The inspectors also witnessed the test and/or reviewed the test data, to verify that test results adequately demonstrated restoration of the affected safety function(s). The inspectors verified that PMT activities were conducted in accordance with applicable WO instructions, or procedural requirements, including SPP-6.3, Post-Maintenance Testing, and MMDP-1, Maintenance Management System. Furthermore, the inspectors reviewed problems associated with PMTs that were identified and entered into the CAP.

  • Common: PMT for replacement of A3 EECW Pump, in accordance with 3-SI-4.5.C.1(2), EECW Pump Operation; 0-SI-4.5.C.1(4), EECW Annual Flow Rate Test; 0-SI-3.1.11, EECW Pump Baseline Data Acquisition and Evaluation; and Work Order 09-715933-003, Remove A3 EECW Pump for Inspection
  • Unit 2: PMT for Control Rod Drive Hydraulic Control Unit Insert Riser Isolation Valve, 2-ISV-085-612/3455, per WO 08-712349-000 and Maintenance Procedures MCI-0-000-GTV001, General Maintenance Instructions for Gate Valves; MCI-0-000-PCK001, General Maintenance Instructions for Valve Packing; and MSI-0-000-PLG001, Installation of Freeze Seals.
  • Unit 2: PMT for replacement of the motor on the Core Spray Pump 2D, in accordance with 2-SR-3.5.1.6(CS II-Comp), Core Spray Loop II Comprehensive Pump Test and Work Orders 07-721562-002, -003, -005 and -007.
  • Unit 1: PMT for Modification/Replacement of Unit 2 Loop II Residual Heat Removal Service Water Heat Exchanger Outlet Valves, 2-FCV-023-46 and -52, per WOs 07-722378-008, -012, and -014, and procedures ECI-0-000-MOV009, Testing of Motor Operated Valves Using MOVATS Universal Diagnostic System (UDS) and Viper 20; 2-SI-4.5.C.1(3), RHRSW Pump and Header Operability and Flow Test; MCI-0-023-VLV001, RHR Service Water Motor Operated Valves 1/2-FCV-23-34, -40, -46, and 52 Disassembly, Inspection, Rework, and Reassembly; and MCI-0-000-PCK001, Generic Maintenance Instruction for Valve Packing.
  • Unit 2: PMT for Replacement of Loop II RHR Pump Motors in accordance with 2-SR-3.5.1.6 (RHR II-COMP), RHR Loop II Comprehensive Pump Test, Work Orders 07-721570-002, -005, and -006 and Work Orders 07-721571-002, -005, and -007.

b. Findings

No findings of significance were identified.

1R20 Refueling and Other Outage Activities

.1 Unit 2 Scheduled Refueling Outage (U2C15)

a. Inspection Scope

During April 25 to June 26, 2009, the inspectors examined critical outage activities to verify that they were conducted in accordance with TS, applicable procedures, and the licensee's outage risk assessment and management plans through the end of the reporting period. Some of the more significant inspection activities conducted by the inspectors were as follows:

Outage Risk Assessment Prior to the Unit 2 Cycle 15 (U2C15) refueling outage that began on April 25, the inspectors attended outage risk assessment team meetings and reviewed the Outage Risk Assessment Report to verify that the licensee had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing an outage plan that assured defense-in-depth of safety functions were maintained. The inspectors also reviewed the daily U2C15 Refueling Outage Reports, including the ORAM Safety Function Status, and regularly attended the twice a day outage status meetings. These reviews were compared to the requirements in licensee procedure SPP-7.2, Outage Management, SPP-7.3, Work Activity Risk Management Process, and TS. These reviews were also done to verify that for identified increased risk significant conditions, due to equipment availability and/or system configurations, contingency measures were identified and incorporated into the overall outage and contingency response plan. Furthermore, the inspectors frequently discussed risk conditions and designated protected equipment with Operations and outage management personnel to assess licensee awareness of actual risk conditions and mitigation strategies.

Shutdown and Cooldown Process The inspectors witnessed the shutdown and cooldown of Unit 2 in accordance with licensee procedures SPP-12.1, Conduct of Operations; 2-GOI-100-12A, Unit Shutdown from Power Operations to Cold Shutdown and Reduction in Power During Power Operations; and 2-SR-3.4.9.1(1), Reactor Heatup or Cooldown Rate Monitoring.

Decay Heat Removal The inspectors reviewed licensee procedures 2-OI-74, Residual Heat Removal System (RHR); 2-OI-78, Fuel Pool Cooling and Cleanup System; and Abnormal Operating Instruction 0-AOI-72-1, Alternate Decay Heat Removal System Failures; and conducted a main control room panel and in-plant walkdowns of system and components to verify correct system alignment. In addition, the inspectors reviewed controls implemented to ensure that outage work was not impacting the ability of operators to operate spent fuel pool cooling, RHR shutdown cooling, and/or ADHR system. Furthermore, the inspectors conducted several walkdowns of the ADHR system during operation with the fuel pool gates removed.

Critical Outage Activities The inspectors examined outage activities to verify that they were conducted in accordance with TS, licensee procedures, and the licensee's outage risk control plan. Some of the more significant inspection activities accomplished by the inspectors were as follows:

18 Enclosure

  • Reviewed and walked down selected safety-related equipment clearance orders (e.g., Equipment Clearance Order 0-TO-2009-0001, Clearance 0-067-0010, for Cutout and Replacement of 1-SHV-67-655, North Header Supply to NE Core Spray Room Cooler).
  • Verified RCS inventory controls, especially during evolutions involving operations with the potential to drain the reactor vessel (OPDRV) controlled per 2-POI-200.5
  • Verified electrical systems availability and alignment
  • Monitored important control room plant parameters (e.g., RCS pressure, level, flow, and temperature) and TS compliance during the various shutdown modes of operation, and mode transitions
  • Evaluated implementation of reactivity controls
  • Reviewed control of containment penetrations and overall integrity
  • Examined foreign material exclusion controls particularly in proximity to and around the reactor cavity, equipment pit, and spent fuel pool
  • Conducted tours of the MCR, reactor building, refueling floor and drywell Reactor Vessel Disassembly and Refueling Activities The inspectors witnessed selected activities associated with reactor vessel disassembly, and reactor cavity flood-up and drain down in accordance with 2-GOI-100-3A, Refueling Operations (Reactor Vessel Disassembly and Floodup). Also, on numerous occasions, the inspectors witnessed fuel handling operations during the three Unit 2 reactor core fuel shuffles performed in accordance with TS and applicable operating procedures, such as GOI-100-3A, Refueling Operations (In Vessel), GOI-100-3B, Operations in the Spent Fuel Pool, and GOI-100-3C, Fuel Movement Operations During Refueling. The inspectors verified specific fuel movements as delineated by the Fuel Assembly Transfer Sheets (FATF).

Torus and Drywell Closeout On May 30, the inspectors reviewed the licensee's final closure of the Unit 2 suppression pool in accordance with 2-GOI-200-2, Primary Containment Initial Entry and Closeout, and performed an independent detailed closeout inspection of the Unit 2 torus.

The inspectors conducted several independent detailed closeout inspections of the Unit 2 drywell prior to and ending on June 19. The inspectors also reviewed and verified the licensee's conduct of 2-GOI-200-2.

Restart Activities The inspectors specifically conducted the following:

- Attended the restart Plant Oversight Review Committee meetings

- Witnessed heatup and pressurization of Unit 2 reactor pressure vessel in accordance with 2-SI-3.3.1.A, ASME Section XI System Leakage Test of the Reactor pressure Vessel and Associated Piping

- Reviewed and verified completion of selected items of 0-TI-270, Refueling Test Program, Attachment 2, Startup Review Checklist

19 Enclosure - Reviewed 2-SR-3.6.1.1.1(OPT-A) Primary Containment Total Leak Rate - Option A, Revision 6

- Witnessed Unit 2 criticality and/or power ascension per 2-GOI-100-1A, Unit Startup and Power Operation, for the startups on June 8, 15, and 20. Also witnessed the Unit 2 shutdowns on June 11 and 16.

- Witnessed and reviewed Unit 2 RCS heatup and pressurization per 2-SR-3.4.9.1, Reactor Heatup and Cooldown Rate Monitoring, for the startups conducted on June 8, 15, and 20. Also witnessed the subsequent RCS cooldowns following the shutdowns on June 11 and 16.

Corrective Action Program The inspectors reviewed PERs generated during U2C15 and attended PER Screening Committee and Corrective Action Review Board meetings to verify that initiation thresholds, priorities, mode holds, operability concerns and significance levels were adequately addressed. Resolution and implementation of corrective actions of several PERs were also reviewed for completeness.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors witnessed portions and/or reviewed completed test data for the following five surveillance tests of risk-significant and/or safety-related systems to verify that the tests met TS surveillance requirements, UFSAR commitments, and in-service testing and licensee procedure requirements. The inspectors' review confirmed whether the testing effectively demonstrated that the SSCs were operationally capable of performing their intended safety functions and fulfilled the intent of the associated surveillance requirement.

In-Service Tests:

  • 1-SR-3.5.1.6(CS I), Quarterly CS System Flow Rate Test Loop I Routine Surveillance Tests
  • 0-SR-3.8.1.9(D), Diesel Generator D Emergency Unit 2 Load Acceptance Test
  • 2-SR-3.1.4.1, Scram Insertion Times
  • 2-SR-3.4.3.2, Main Steam Relief Valve Manual Cycle Test Containment Isolation Valve Tests

20 Enclosure

b. Findings

No findings of significance were identified.

Cornerstone:

Emergency Preparedness 1EP6 Drill Evaluation

a. Inspection Scope

During the report period, the inspectors observed an Emergency Preparedness (EP)drill that contributed to the licensee's Drill/Exercise Performance (DEP) and Emergency Response Organization (ERO) performance indicator (PI) measures on April 7, 2009, to identify any weaknesses and deficiencies in classification, notification, and protective action recommendation (PAR) development activities. The inspectors observed emergency response operations in the simulated control room and certain Emergency Response Facilities to verify that event classification and notifications were done in accordance with EPIP-1, Emergency Classification Procedure and other applicable Emergency Plan Implementing Procedures. The inspectors also attended the licensee critique of the drill to compare any inspector-observed weakness with those identified by the licensee in order to verify whether the licensee was properly identifying weaknesses.

b. Findings

No findings of significance were identified.

RADIATION SAFETY

Cornerstone:

Occupational Radiation Safety (OS)2OS1 Access Control To Radiologically Significant Areas

a. Inspection Scope

Access Control: The inspectors evaluated licensee performance in controlling worker access to radiologically significant areas and monitoring jobs in-progress associated with the U2C15 refueling outage. The inspectors directly observed implementation of administrative and physical radiological controls; evaluated radiation worker (radworker)and radiation protection technician (RPT) knowledge of and proficiency in implementing radiation protection requirements; and assessed worker exposures to radiation and radioactive material.

During facility tours, the inspectors directly observed postings and physical controls for radiation areas, high radiation areas (HRAs), and potential airborne radioactivity areas established within the radiation control area (RCA) of the Unit 2 (U2) drywell, Unit 1 (U1),

U2, and Unit 3 (U3) reactor buildings, U1/U2/U3 turbine building, and radioactive waste (radwaste) processing and storage locations. The inspectors independently measured radiation dose rates or directly observed conduct of licensee radiation surveys for selected RCA areas. Results were compared to current licensee surveys and assessed against established postings and Radiation Work Permit (RWP) controls. Licensee key control and access barrier effectiveness were evaluated for selected U1, U2, and U3 21 Enclosure Locked High Radiation Area (LHRA) and Very High Radiation Area (VHRA) locations. Changes to procedural guidance for LHRA and VHRA controls were discussed with radiation protection (RP) supervisors.

Controls and their implementation for storage of irradiated material within the spent fuel pool (SFP) were reviewed and discussed in detail. Established radiological controls were evaluated for selected U2C15 outage tasks including transverse in-core probe under-vessel work, control rod drive accumulator maintenance, diving activities associated with steam dryer work, in-service inspection, scaffolding support, insulation, shielding, motor replacements In addition, licensee controls for areas where dose rates could change significantly as a result of plant shutdown and refueling operations were reviewed and discussed.

For selected tasks, the inspectors attended pre-job briefings and reviewed RWP details to assess communication of radiological control requirements to workers. Occupational workers' adherence to selected RWPs and RPT proficiency in providing job coverage were evaluated through direct observations and interviews with licensee staff. Electronic dosimeter (ED) alarm set points and worker stay times were evaluated against area radiation survey results for drywell and refueling floor activities.

The inspectors evaluated the effectiveness of radiation exposure controls, including air sampling, barrier integrity, engineering controls, and postings through a review of both internal and external exposure results. Worker exposure as measured by ED and by licensee evaluations of skin doses resulting from discrete radioactive particle or dispersed skin contamination events during current U2C15 outage activities were reviewed and assessed. For HRA tasks involving significant dose rate gradients, e.g. steam dryer repair activities by divers in the fuel pool, the inspectors evaluated the use and placement of whole body and extremity dosimetry to monitor worker exposure. The inspectors also reviewed and discussed selected whole-body count analyses conducted during 2008 and the current U2 refueling outage.

The inspectors walked-down the Independent Spent Fuel Storage Installation (ISFSI) facility, observing the physical condition of the casks, radiological postings, and barriers. The inspectors performed independent gamma radiation surveys of the area and reviewed gamma radiation surveys of the ISFSI facility performed by licensee personnel. Inspectors compared the independent survey results to previous surveys and against procedural and TS limits. The inspectors evaluated implementation of radiological controls, including labeling and posting, and discussed controls with RP staff.

Environmental monitoring results for direct radiation from the ISFSI were reviewed and inspectors observed the placement and physical condition of thermoluminescent dosimeters (TLDs) around the facility.

Radiation protection activities were evaluated against the requirements of UFSAR Section 12; TS Sections 5.4 and 5.7; 10 Code of Federal Regulations (CFR) Parts 19 and 20; and approved licensee procedures. Radiological control activities for ISFSI areas were evaluated against 10 CFR Part 20, 10 CFR Part 72, and TS details. Records reviewed are listed in Section 2OS1 of the report Attachment.

Problem Identification and Resolution: Licensee Corrective Action Program (CAP) documents associated with access control to radiologically significant areas were reviewed and assessed. This included review of selected PERs related to radworker 22 Enclosure and RPT performance. The inspectors evaluated the licensee's ability to identify, characterize, prioritize, and resolve the identified issues in accordance with procedure SPP-3.1, Corrective Action Program, Rev. 15. The inspectors also evaluated the scope of the licensee's internal audit program and reviewed recent assessment results. Licensee CAP documents reviewed are listed in Section 2OS1 of the report Attachment.

The inspectors completed the 21 required line-item samples described in Inspection Procedure (IP) 71121.01. The inspectors also completed the radiation protection line-item sample activities specified in IP 60855.1.

b. Findings

Introduction:

A self-revealing Green NCV of TS 5.4.1, Procedures, was identified for a failure to comply with the requirements of Radiation Work Permit (RWP) 09270081, as required by procedure RCI-9.1, Radiation Work Permits.

Description:

On May 15, 2009, a machinist received a briefing on RWP 09270081, U2C15 Reactor Building Movats (Various Dress), with an electronic dosimeter (ED) dose alarm setpoint of 50 millirem (mrem) and a dose rate setpoint of 80 millirem per hour (mrem/hr). Based on the work location communicated to RP by the machinist, he was briefed on the radiological conditions in the HPCI room, located adjacent to the U2 SE Quad on the 519' elevation. The anticipated dose rates in the HPCI room were < 1 mrem/hr general area, with some localized areas < 5 mrem/hr. The RWP required the worker to review appropriate survey data prior to entry and did not allow entry into high radiation areas.

The worker then proceeded to the U2 519' SE Quad and, instead of entering the HPCI room, passed through a high radiation area (HRA) swing gate and entered a posted HRA in order to look for the valve he was tasked to work on, located near the RHR pumps. Shortly after entering the HRA, the worker received an unanticipated dose rate alarm of 84 mrem/hr, identified when he logged-off the RWP. Because the worker did not hear the ED alarm, he continued to work in the posted high radiation area, unaware of the radiological conditions because they had not been covered during his briefing.

Actual radiological conditions were 30-40 mrem/hr general area, and 50 mrem/hr at 30 cm from the RHR pumps. Based on the briefed radiological conditions, it was expected that the worker would receive 1-2 mrem to perform the valve work; because he performed the work in a significantly higher dose rate field than had been briefed, he received a total dose of 19 mrem.

The machinist had successfully completed radworker training, which detailed the different types of radiological postings/barriers and requirements for entry into areas such as HRAs. Because a swing gate served as a physical barrier to inadvertent entry into the HRA on the U2 519' SE Quad, the worker missed an opportunity to self-check his actions prior to entry into the area.

Analysis:

The inspectors determined that the failure to follow the requirements of RWP 09270081 was a performance deficiency. This finding was greater than minor because it was associated with the Occupational Radiation Safety Cornerstone attribute of Program and Process (Exposure Control) and adversely affected the cornerstone objective of ensuring adequate protection of worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation.

23 Enclosure The finding was evaluated using the Occupational Radiation Safety SDP and determined to be of very low safety significance (Green) because it was not related to As Low As Reasonably Achievable (ALARA) planning, nor did it involve an overexposure or substantial potential for overexposure, and the ability to assess dose was not compromised. The cause of this finding was directly related to the cross-cutting aspect of work practices in the Human Performance area, because the machinist failed to use self-checking prior to passing through the swing gate into the posted high radiation area (H.4.a).

Enforcement:

Technical Specifications 5.4.1, Procedures, required the licensee to implement the procedures contained in Regulatory Guide (RG) 1.33, Rev. 2, Appendix A. RG 1.33, Appendix A, Section 7.e. which required written procedures for Radiation Protection, including access control to radiation areas and a radiation work permit system. Licensee procedure RCI-9.1, Radiation Work Permits, Rev. 57, required radworkers to use the appropriate RWP for entries into the RCA and to comply with all RWP special instructions. RWP 09270081, U2C15 Reactor Building Movats (Various Dress), Worker Instruction Number (No.) 3 required workers to review appropriate survey data prior to entry and Worker Instruction No. 4 specified no entry into high radiation areas on this RWP. Contrary to this, on May 15, 2009, a machinist passed through a swing gate and entered a posted high radiation area on RWP 09270081 without having reviewed appropriate survey data for the area, contrary to the RWP Worker Instructions Nos. 3 and 4. Because this finding was determined to be of very low safety significance and has been entered into the licensee's CAP (PER 171375), this violation is being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy: NCV 05000259,260,296/2009003-03, "Failure to Comply with the Requirements of an RWP by Entering a Posted High Radiation Area." 2OS2 As Low As Reasonably Achievable Planning and Controls

a. Inspection Scope

As Low As Reasonably Achievable: The inspectors evaluated ALARA program guidance and implementation for ongoing tasks associated with the U2C15 refueling outage. In addition, the inspectors evaluated the post-outage ALARA activities associated with the Unit 1 Cycle 7 (U1C7) refueling outage. The inspectors reviewed and discussed with licensee staff various ALARA work plan documents, including dose estimates and prescribed ALARA controls for selected outage work activities expected to incur significant collective doses. The inspectors reviewed the implementation of dose-reduction initiatives for high person-rem expenditure tasks. The inspectors evaluated these elements of the ALARA program for consistency with the methods and practices delineated in applicable licensee procedures.

The inspectors evaluated the implementation and effectiveness of ALARA planning and program initiatives during work in progress. The inspectors made direct field observations of U2 work activities involving the steam dryer repair, specifically diving operations including diver preparation, supervision, dosimetry placement and removal, and work area radiation surveys. The inspectors observed work on the CRD accumulators, scaffold erection, and in-service inspection. The inspectors interviewed radiation workers and RPT staff to assess their understanding of dose reduction initiatives and their current and expected final accumulated occupational doses at completion of the task.

24 Enclosure Projected RWP dose expenditure estimates from U2C15 and U1C7 refueling outage efforts were compared to actual dose expenditures, and noted differences were discussed with cognizant ALARA staff. Changes to dose budgets relative to changes in job scope were identified and discussed. The inspectors attended pre-job briefings and evaluated the communication of ALARA goals, RWP requirements, and industry lessons-learned to job crew personnel.

The inspectors evaluated the implementation and effectiveness of selected program initiatives with respect to source-term reduction. The inspectors reviewed source term reduction plan that would duplicate many of the source term reduction efforts that have been applied to Unit 1 for the other two units. The inspectors noted that many items in the source term reduction plan had been eliminated or deferred past calendar year (CY) 2014 into the next 5-year planning cycle. The inspectors discussed the potential impacts of the eliminations and deferrals with RP management. The effectiveness of selected shielding packages installed for the current outage was assessed through completion of independent radiation surveys and comparison to applicable licensee survey records and expected planning data.

The plant collective exposure histories for CY 2005, 2006 and 2007, taken from data reported to the NRC pursuant to 10 CFR 20.2206(c), were reviewed and discussed with licensee staff, as were established goals for reducing collective exposure. The inspectors reviewed the applicable guidance and examined dose records of declared pregnant workers during CY 2007 and 2008 to evaluate current gestation doses for declared pregnant workers.

ALARA activities were evaluated against the requirements specified in 10 CFR 19.12; 10 CFR Part 20, Subparts B, C, F, G, H, and J; and approved licensee procedures. In addition, licensee performance was evaluated against RG 8.8, Information Relevant to Ensuring that Occupational Radiation Exposures at Nuclear Power Stations will be As Low As Reasonably Achievable, and RG 8.13, Instruction Concerning Prenatal Radiation Exposure. Procedures and records reviewed within this inspection area are listed in Sections 2OS1 and 2OS2 of the report Attachment.

Problem Identification and Resolution: The inspectors reviewed the licensee corrective action documents associated with ALARA activities. The inspectors evaluated the licensee's ability to identify, characterize, prioritize, and resolve the identified issues in accordance with the corrective action program. Specific self-assessments, audits, and PERs reviewed and evaluated in detail for this inspection area are identified in Section 2OS2 of the report Attachment.

The inspectors completed the 15 required line-item samples and 14 optional line-item samples, for a total of 29 line-item samples, as described in IP 71121.02.

b. Findings

No findings of significance were identified.

Cornerstone:

Public Radiation Safety 2PS1 Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems

a. Inspection Scope

Groundwater Monitoring: The inspectors discussed current and future programs for onsite groundwater monitoring with licensee staff, including number and placement of monitoring wells and identification of plant systems with the most potential for contaminated leakage. The inspectors also reviewed procedural guidance for identifying and assessing onsite spills and leaks of contaminated fluids. The inspectors determined that no contaminated spills, leaks, or unplanned releases had occurred since the last inspection in this area.

Analyses are performed for tritium and, for selected samples, hard-to-detect radionuclides for both groundwater and drinking water samples. No levels exceeding the EPA drinking water limit of 20,000 picoucuries per liter (corresponding to 4 millirem per year to a member of the public) have been identified in the onsite or offsite environs.

b. Findings

No findings of significance were identified.

2PS2 Radioactive Material Processing and Transportation

a. Inspection Scope

Waste Processing and Characterization: The inspectors reviewed the plant's solid radioactive waste system description in the UFSAR and process control program (PCP). The most recent radiological effluent release report was reviewed for information on the types and amounts of waste disposed. The scope of the licensee's audit program was reviewed to verify that it met the requirements of 10 CFR 20.1101(c). The inspectors walked down the accessible portions of the liquid and solid radioactive waste processing systems to verify and assess that the current system configuration and operation agreed with the UFSAR and PCP. The use of video cameras to monitor batch tank levels was also discussed with selected radwaste and operations representatives.

The inspectors reviewed the radiological operating report for any documented changes to the radwaste processing systems and discussed observations from a walkdown of the systems with selected radwaste and operations representatives.

The inspectors reviewed the plant's process for transferring radioactive resin and sludge discharges into shipping/disposal containers to determine if appropriate waste stream mixing and/or sampling procedures and methodology for waste concentration averaging provided representative samples of the waste product for waste classification purposes. The inspectors reviewed current 10 CFR 61 analysis results and the procedures for obtaining the samples to support the analysis. The scaling factors used for radioactive waste streams and calculations used for determining the amount of hard to detect nuclides were reviewed. The program was reviewed to verify compliance with 10 CFR 61.55-56 and Appendix G of 10 CFR 20.

The inspector reviewed the program for provisions that would ensure that the waste stream composition accounted for changes in operational parameters and would remain valid between required periodic updates.

26 Enclosure Transportation: The inspectors observed the preparation and shipment of resin to a vendor facility. The observations included packaging, surveying, labeling, placarding, vehicle checks, driver's briefing and emergency instructions, a review of shipping papers provided to the driver, and licensee final verification of shipment readiness. The inspectors observed two LSA-II type shipments, one involved a cask of dewatered condensate resin and the other was for contaminated plant protective clothing. The inspectors reviewed selected shipping documentation for shipments that had occurred from January 2008 to May 2009. The inspectors reviewed the QA surveillance documentation verifying compliance with the Certificate of Compliance for a Type B package that included dewatered resin. The inspectors observed, interviewed and reviewed the training records of the radwaste workers who were involved in the selected shipments.

Transportation program implementation was reviewed against regulations detailed in 10 CFR Part 20, 10 CFR Part 71, 49 CFR Parts 172-178; as well as the guidance provided in NUREG-1608. Training activities were assessed against 49 CFR Part 172 Subpart H. Documents reviewed during the inspection are listed in Section 2PS2 of the report Attachment.

Problem Identification and Resolution: Select PERs and self-assessments were reviewed in detail and discussed with cognizant licensee personnel. The inspectors assessed the licensee's ability to characterize, prioritize, and resolve the identified issues in accordance with licensee procedure SPP-3.1, Corrective Action Program, Rev.

15. Documents reviewed for problem identification and resolution are listed in Section 2PS2 of the report Attachment.

The inspectors completed the six required line-item samples described in IP 71122.02.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification

.1 Cornerstone:

Mitigating Systems Safety System Functional Failures

a. Inspection Scope

The inspectors reviewed the licensee's procedures and methods for compiling and reporting the Performance Indicators (PI) listed below, including procedure SPP-3.4, Performance Indicator for NRC Reactor Oversight Process for Compiling and Reporting PIs to the NRC. The inspectors reviewed the raw data for the PIs listed below for the second quarter of 2008 through first quarter 2009 and discussed the methods for compiling and reporting the PIs with cognizant licensing, engineering, and maintenance rule personnel. The inspectors compared the licensee's raw data against graphical representations and specific values reported to the NRC in the second quarter 2009 PI report to verify that the data was correctly reflected in the report.

27 Enclosure The inspectors also reviewed the past history of PERs for any that might be relevant to problems with the PI program. The inspectors reviewed Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, to verify that industry reporting guidelines were applied.

  • Unit 1 Safety System Functional Failures
  • Unit 2 Safety System Functional Failures
  • Unit 3 Safety System Functional Failures

b. Findings

No findings of significance were identified.

.2 Cornerstone:

Occupational Radiation Safety Occupational Exposure Control Effectiveness

a. Inspection Scope

The inspectors reviewed PI data collected from April 1, 2008, through March 31, 2009, for the Occupational Exposure Control Effectiveness PI. For the reviewed period, the inspectors assessed CAP records to determine whether HRA, VHRA, or unplanned exposures, resulting in TS or 10 CFR 20 non-conformances, had occurred during the review period. In addition, the inspectors reviewed selected personnel contamination event data, internal dose assessment results, and ED alarms for cumulative doses and/or dose rates exceeding established set-points. The reviewed data were assessed against guidance contained in NEI 99-02. The reviewed documents relative to these PI reviews are listed in Sections 2OS1, 2OS2, and

4OA1 of the report Attachment.

b. Findings

No findings of significance were identified.

.3 Cornerstone:

Public Radiation Safety Radiological Control Effluent Release Occurrences

a. Inspection Scope

The inspectors reviewed the Radiological Control Effluent Release Occurrences PI results for the period of April 1, 2008 through March 31, 2009. For the assessment period, the inspectors reviewed cumulative doses to the public, gaseous and liquid effluent release permits, and selected PERs related to effluent control. The inspectors also reviewed licensee procedural guidance for collecting and documenting PI data. The reviewed data were assessed against guidance contained in NEI 99-02. Documents reviewed are listed in Section

4OA1 of the report Attachment.

b. Findings

No findings of significance were identified.

28 Enclosure

4OA2 Identification and Resolution of Problems

.1 Review of items Entered into the Corrective Action Program:

As required by Inspection Procedure 71152, "Identification and Resolution of Problems," and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensee's CAP. This review was accomplished by reviewing daily PER report summaries, periodically attending Corrective Action Review Board (CARB) meetings and periodically attending PER Screening Committee (PSC) meetings.

.2 Semi-Annual Review to Identify Trends

a. Inspection Scope

As required by Inspection Procedure 71152, the inspectors performed a review of the licensee's CAP implementation and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors' review included the results from daily screening of individual PERs (see Section 4OA2.1 above), licensee trend reports and trending efforts, and independent searches of the PER database and WO history. The review also included issues documented outside the normal CAP in system health reports, corrective maintenance WOs, component status reports, site monthly meeting reports and maintenance rule assessments. The inspectors' review nominally considered the six-month period of January 2009 through June 2009, although some PER database and WO searches expanded beyond these dates. Furthermore, the inspectors verified that adverse or negative trends identified in the licensee's PERs, periodic reports and trending efforts were entered into the CAP. Inspectors also interviewed the appropriate licensee management.

b. Findings and Observations

Inspectors reviewed the licensee's integrated trend review (ITR) program and the implementation of the program. As documented in Performance Improvement Department Procedure (PIDP) PIDP-11, PER Trending, trend reviews were to be conducted each quarter. The intent of this review was to identify the top organizational issues, both at the department and site level, and to report on the progress being made to resolve them. The inspectors determined that the licensee's trending program, in general, has shown improvement from previous inspections. The Integrated Trend Review Meeting was scheduled well in advance and departments were actively participating in the process. It should also be noted that a new procedure, PDIP-12, Integrated Trend Review, has been issued during this period, to provide additional guidance on conducting trending.

The inspectors noted areas in the trending program that warranted additional attention by the licensee, as follows:

  • Some departmental negative trends that were continuing from previous ITRs relied on existing PERs or were closed to existing programs, without conducting a thorough evaluation if the existing PERs or programs were adequate to correct the problem. For example, several negative trends identified in the radiation protection department (e.g., contaminated area, number of hot spots, number of 29 Enclosure catch containments), were identified and new PERs were written. However, these PERs were closed to existing programs which have not been effective in reversing these trends. It was not apparent that an adequate evaluation was being conducted to ensure that the existing PER corrective actions were being effective, that these actions were timely enough or that criteria was being established where additional actions were needed (i.e., when an additional PER would be required).
  • Department trend reports contained issues identified by external organizations, but in general did not address why the line organization did not identify these issues as required by PIDP-11. The licensee initiated PER 171857.

The inspectors conducted an independent review to identify potential negative trends, and identified several notable trends, as follows:

  • A potential adverse trend was identified in conducting adequate PMTs. Some examples included: Unit 2 HPCI steam admission valve was repaired to correct seat leakage, but no seat leakage PMT was conducted (PER 161154); RHR HX outlet valves exhibited high vibrations causing repetitive failures, but following replacement of these valves vibration levels are not measured or evaluated (PER 171914); EECW manual isolation valve was replaced, but adequate flow to the room cooler was not verified during the PMT (PER 170650); and pressure testing following replacement of a manual isolation valve in the control rod drive system was not conducting at normal operating pressure (PER 172233). The licensee initiated PER 173055 to address this trend.
  • The licensee established a PER corrective action closure review committee to ensure that corrective actions were being completed as described in the original action statement and properly documented. Over 70 PERs have been generated by this committee to document problems with PER action closures. In general, these PERs corrected the specific condition described, but no trend PER has been generated to evaluate and correct this trend in inappropriate approval of inadequate PER actions. The licensee initiated PER 175822 to address this trend.
  • There have been several instances that inspectors have identified direct physical contact of safety related piping and/or conduits on other systems, structures or components. Examples included 1A Core Spray pump motor heater conduit against the 1A CS pump casing vent, 1C RHR pump seal leakage pipe against the 1C RHR pump suction vent line, 1A RHR pump seal water vent valve against 1A RHR pump seal leakage piping, and 1B CS cyclone separator tubing against the 1B CS pump pedestal. The licensee initiated PER 173522 to address this trend.

No violations of NRC requirements were identified.

.3 Focused Annual Sample Review - Risk Management

a. Inspection Scope

30 Enclosure The inspectors reviewed the specific corrective actions associated with the licensee's risk management trending PERs 160566, 167965, 170977, and other related PERs. Additionally, the inspectors reviewed corrective actions that resulted in issuing the new procedure SPP-7.3, Work Activity Risk Management Process; and a revision to existing procedure SPP-7.1, On-Line Work Management. Inspectors also reviewed BP-336, Risk Determination and Risk Management. Furthermore, the inspectors interviewed daily scheduling, outage, and operations risk management personnel.

b. Findings and Observations

Introduction:

The inspectors identified an issue associated with the possible omission of certain risk significant systems from the licensee's routine assessment of online risk that was required by 10 CFR Part 50.65 (a)(4), "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants.

" This issue is being characterized as an unresolved item (URI).

Description:

Several systems identified as risk significant by the licensee's MR Program, and listed in Table 2, Initiators and System Dependency, of the "Risk Informed Inspection Notebook for Browns Ferry Nuclear Plant Units 1 and 2", did not appear to be considered as part of the licensee's routine online risk assessment. The inspectors observed that the following risk significant systems identified in Table 2 did not appear to be evaluated for on-line risk impact by the licensee: Raw Cooling Water (RCW), Fuel Oil Transfer, Emergency Diesel Generator (EDG) Room Ventilation (i.e., exhaust fans), Plant Control Air, Drywell Control Air, and Containment Ventilation. Furthermore, examples of risk significant systems identified as risk significant by the licensee's MR Program that did not appear to be assessed for online risk were as follows: RCW, EDG Room Ventilation, EDG Starting Air, and the Fuel Oil Transfer system.

To address the inspectors' concern regarding the assessment of online risk for all risk significant systems the licensee initiated PER 169904. As part of the corrective actions for PER 169904, the licensee committed to review Table 2 of risk significant systems against the list of risk significant systems as determined by the new Browns Ferry PRA model that was being developed, once it has been peer reviewed and approved. At which point the licensee's maintenance rule and on-line risk management tools would be updated accordingly.

This issue of concern requires additional information from the licensee. Such as, whether the MR and Table 2 designations of risk significant systems are appropriate, and how the current online risk assessment tools do or do not scope or bound the impact on risk associated with the unavailability of the aforementioned systems. Consequently, pending additional information from the licensee and further review by the NRC, this issue will be identified as URI 05000259, 260, 296/2009003-04, Inadequate Scoping of Risk Significant Systems for Online Risk Assessment.

Observations The inspectors had the following observations:

PERs 160566, 167965, and 170977

31 Enclosure The evaluation, development, and implementation of corrective actions for inadequate communications of plant risk were untimely and remained incomplete. As a potential adverse trend, this issue was discussed with the licensee in December 2008 and documented in NRC Integrated Inspection Report 05000259/2008005, 05000260/2008005 and 05000296/2008005, issued in January 2009. The licensee initiated PER 160566 on January 8, 2009 to document this potential trend in plant risk management where there were numerous instances in which risk assessments from ORAM, the shutdown plant outage risk assessment management software, and SENTINEL, the operating plant computer based risk management model, did not accurately reflect the actual plant equipment configuration. The corrective action to evaluate the potential trend was initiated on February 6, 2009. Subsequently, the licensee extended the PER citing resource re-allocation due to unplanned forced outages. On April 7, 2009, the licensee determined that a trend existed for not meeting expectations for clear communications of plant risk such as: conflicting risk levels on different site documents; incorrect information related to equipment out of service in the plan of the day; and inadequate transition from ORAM to SENTINEL risk model during unit restart. On that same day, PER 167965 was initiated to develop a corrective action plan for this trend. On May 6, 2009, PER 167965 was prematurely closed with incomplete actions taken, contrary to actions previously discussed with NRC inspectors. On May 11, 2009, the licensee initiated a third PER 170977 to document additional corrective actions. Inspectors discussed their concern with further prolonging corrective actions and the licensee initiated PER 171722 for inadequate and untimely corrective actions.

SPP-7.3, Work Activity Risk Management Process Inspectors reviewed newly developed licensee procedure SPP-7.3, Work Activity Risk Management Process, to evaluate the corrective actions documented in PER 167965.

The inspectors made the following observations:

  • The relocation of risk management action (RMA) guidance from SPP-7.1, On-Line Work Management, to SPP-7.3 was incomplete. SPP-7.3, Appendix E lists RMAs available for various levels of risk, but did not include all of the RMAs in SPP-7.1, Section 3.5.1.c. Additionally, SPP-7.1, Appendix J contained critical evolution meeting guidance that in itself was an RMA, and was not contained in SPP-7.3. The licensee's site and corporate (SPP administrators) personnel agreed with inspector observations and intend to revise the two SPPs in accordance with their corporate procedure process.
  • Risk management review forms to support the new SPP-7.3 procedure had still not been developed four weeks after the procedure became effective. The licensee stated that implementation of the procedure was planned to be a phased-in effort coinciding with the work week development process, and initiated an action as part of PER 170977 to track the development of the forms.

BP-336, Risk Determination and Risk Management With approximately 11 weeks remaining until BP-336 would be phased out and deactivated, inspectors noted that Operations guidance associated with plant risk matrices and protected equipment (which the operations department intended to maintain) did not have a prospective home in another procedure or similar guidance 32 Enclosure document. Inspectors also noted that the licensee had not documented this concern in their CAP, and therefore a documented plan of action was not in place. The licensee initiated an action as part of PER 170977.

Equipment Out of Service (EOOS) Risk Assessment Tool

During discussions with the licensee concerning their development of new risk management and assessment tools, inspectors noted that with the planned phasing in of the new PRA-based EOOS software near the end of 2009 and the planned phasing out of SENTINEL, there was a lack of risk assessment tool coverage for Mode 3 Hot Shutdown. The licensee agreed that this would be the case until the low power shutdown model was completed in approximately five years which would apply in Modes 1, 2, and 3. The licensee initiated PER 169925 to resolve risk tool coverage for Mode 3 conditions.

4OA3 Event Follow-up

.1 (Closed) LER 05000260/2009-001, Manual Reactor Scram Following Stator Cooling Water Equipment Failure

a. Inspection Scope

On February 16, 2009, the Unit 2 reactor was manually scrammed from 100 percent power due to high main generator stator cooling water (SCW) temperature. The loss of stator water cooling was due to the failure of the SCW temperature controller which caused the temperature control valve (2-TCV-035-0054) to fail open and bypass too much SCW from the SCW heat exchanger. The exact cause of the SCW temperature controller failure was not definitively determined by the licensee. During and following the scram, all safety-related mitigating systems operated as designed, and all operator actions in response to the scram were deemed to be appropriate (see IR 05000260/2009-002, Section 4OA3.1). This LER and its associated PER 163680, including the root cause analysis (RCA), were reviewed by the inspectors.

b. Findings

No new significant findings or violations of NRC requirements were identified. This LER is considered closed.

.2 (Closed) LER 05000259/2009-001, Turbine Trip and Reactor Scram Due to Power Load Unbalance Signal on the Main Generator

a. Inspection Scope

On February 18, 2009, the Unit 1 reactor was automatically scrammed from 100 percent power due to a power load unbalance when the main turbine generator (MTG) output breaker tripped. The Unit 1 MTG protective relays were actuated when a significant quantity of water was blown onto the main generator output isophase buses causing an electrical ground fault. The source of the water was from excessive condensation that had been accumulating in the idle 1B isophase bus duct cooling fan, such that when operators switched from the in-service 1A fan, to the 1B fan, a large quantity of water was entrained and ejected onto the isophase buses. During and following the scram, all 33 Enclosure safety-related mitigating systems operated as designed, and all operator actions in response to the scram were deemed to be appropriate (see IR 05000259/2009-002, Section 4OA3.2). This LER and its associated PER 163815, including the RCA, were reviewed by the inspectors. The inspectors also reviewed previous PERs related to excessive condensation and walked down the Unit 1 isophase bus cooling (IBC) system shortly after the event. Furthermore, the inspectors interviewed the RCA team leader.

b. Findings

This LER is considered closed with one finding identified.

Introduction:

A Green self-revealing finding was identified for a failure to implement corrective actions in a timely manner to address excessive IBC system condensation that resulted in an MTG trip and Unit 1 reactor scram caused by water accumulation in the IBC ductwork, which created an electrical ground fault on the MTG isophase busses.

Description:

A review of work orders from as far back as 1993, by the licensee, determined that plant personnel frequently observed excessive condensation dripping from the IBC system ductwork during winter operating conditions. Alabama winters have frequently included certain days when river water temperatures were very cold, but ambient air was warm and humid (e.g., after a storm front). During these conditions, the IBC coolers would generate considerable quantities of condensed water in the bus ductwork. Excessive condensation dripping from the IBC ductwork seams had been observed and tolerated by the licensee for many years.

In 2006, Unit 1 installed a new IBC system. This new system was designed to have much a higher capacity cooler, along with dual fans vice the original single fan design. The new Unit 1 IBC design was based on the worst case Extended Power Uprate Isophase Bus loading, along with worst case river water temperatures (i.e., during the summer). The licensee determined in their root cause analysis, that the Unit 1 IBC design change did not consider or evaluate the potential adverse implications associated with winter operating conditions. The inspectors verified that the technical considerations required to be evaluated by SPP-9.3, Plant Modifications and Engineering Change Control, for design changes did not require the impact of seasonal environmental changes to be evaluated. However, it was apparent to the licensee and inspectors, that the new design features of the Unit 1 IBC system were more conducive to generating and accumulating larger quantities of condensation during winter operating conditions than the old system. On December 8, 2007, as in previous occasions, plant personnel observed water leaking from the seams of the Unit 1 IBC ductwork and initiated WO 07-727187-000 to correct the problem. However, the WO wasn't worked until October 2008 at which time there was no water to be found. This WO was closed with no work performed. Then, on December 10, 2008, plant personnel again discovered excessive moisture coming out of the seams of the Unit 1 IBC ductwork. This time the abnormal equipment condition was entered into the licensee's CAP as PER 158940 (Level C PER). The inspectors noted that the specific actions to promptly correct the problem recommended by the PER were not implemented prior to the event.

In the purpose section of SPP-3.1, Corrective Action Program, it stated that this SPP established the processes and responsibilities for documenting and resolving problems at the station. This program procedure also addressed safety-related problems required 34 Enclosure to be corrected by 10 CFR 50, Appendix B, Criterion XVI, Corrective Action. The overall purpose of the licensee's CAP was to provide the necessary site standards to ensure that all abnormal equipment conditions entered into the CAP, including non-safety related equipment deficiencies, were resolved. The licensee initiated PER 158940, and designated it as a Level C PER, to ensure that the site standards imposed by SPP-3.1 were implemented and followed to resolve the excessive IBC system condensation. The licensee's failure to implement the actions recommended by PER 158940 in a timely manner was a missed opportunity to prevent the Unit 1 reactor scram of February 18, 2009. During the subsequent event investigation, shortly after the Unit 1 scram, the licensee discovered approximately 35 gallons of water (i.e., condensate) remaining in the IBC ductwork. From this observation and a system walkdown, the licensee concluded that at least this amount of water had originally condensed and collected in the idle 1B IBC fan housing prior to the event. Based on the observed persistent problems with water accumulation in the IBC ductwork, including the multiple WO's and PERs that were written, the inspectors concluded the licensee had many past and recent opportunities to address this condition. It was therefore reasonable to conclude that it was within the licensee's ability to foresee and correct the condition before it resulted in a reactor scram.

Analysis:

The licensee's failure to implement corrective actions in a timely manner, according to the site standard of SPP-3.1, in order to resolve a known abnormal equipment condition involving excessive IBC condensation, was a performance deficiency which directly resulted in an automatic reactor scram. This finding was determined to be greater than minor because it was associated with the initiating events cornerstone attribute of equipment performance, and adversely affected the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during at-power operations. The finding was evaluated using Phase 1 of the At-Power SDP, and was determined to be of very low safety significance (Green) because it did not contribute to both the likelihood of a reactor trip and the likelihood that mitigating equipment or functions were not available.

The cause of this finding was directly related to the cross-cutting aspect of appropriate and timely corrective actions in the area of Problem Identification and Resolution, because the license had identified an abnormal equipment condition related to excessive IBC system condensation for which corrective actions were specified but not carried out (P.1.d).

Enforcement:

Enforcement action does not apply because the performance deficiency did not involve a violation of a regulatory requirement since the IBC system is not safety-related. Because this finding does not involve a violation of regulatory requirements, was entered in the licensee's CAP as PER 163815, and has very low safety significance, it is identified as FIN 05000259/2009003-05, Untimely Actions to Resolve Excessive IBC System Condensation Results in Unit 1 Reactor Scram.

.3 (Closed) LER 05000259/2009002-00, Unexpected Logic Lockout of the Loop II Residual Heat Removal System Pumps

a. Inspection Scope

On March 21, 2009, RHR pumps 1B and 1D automatic start feature was locked out during a surveillance, while RHR pumps 1A and 1C had previously been removed from service for testing. The cause of the lockout was an error in the Core Spray Logic Functional Test procedure that resulted in the installation of a jumper in the wrong logic panel. Operations personnel immediately recognized that the placement of the jumper had rendered the pumps inoperable and entered TS LCO 3.0.3. After approximately one minute, the automatic start function of RHR Pumps 1B and 1D was restored and TS 3.0.3 was exited. Corrective actions included removal of the jumper, revision of the surveillance procedure and placing similar logic functional test procedures on administrative hold until a thorough review could be conducted. This event was reviewed by the inspectors and documented in Inspection Report 05000259/2009-002. NCV 05000259/2009002-02, Inadequate Surveillance Procedure Causes Loss of Unit 1 RHR System Safety Function, was issued as a result of this review. The inspectors reviewed the LER and associated PER 166487 and root cause analysis.

b. Findings

No new significant findings or violations of NRC requirements were identified. This LER is closed.

4OA5 Other Activities

.1 Quarterly Resident Inspector Observations of Security Personnel and Activities

a. Inspection Scope

During the inspection period the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security. These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status reviews and inspection activities.

b. Findings

No significant findings were identified.

4OA6 Meetings, Including Exit

.1 Quarterly Integrated Inspection Report Exit Meeting Summary

On July 6 and 17, 2009, the senior resident inspector presented the inspection results to Mr. Jim Randich, Mr. Don Grissette, and other members of the licensee staff, who acknowledged the findings. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary. No proprietary information was identified.

36 Enclosure

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which met the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as a Non-Cited Violation.

  • TS 5.7.1, requires that each individual or group entering such an area (locked high radiation area) shall possess a device that continuously transmits dose rate information to a remote receiver monitored by radiation protection personnel or be under the surveillance of an individual qualified in radiation protection procedures equipped with a radiation monitoring device that continuously displays dose rates in the area. Contrary to this, on April 15, 2008, a radworker retrieved his ED from the 550 foot elevation of the U3 drywell without being issued another ED, being monitored by a RPT or being accompanied by a RPT with a survey instrument. This event was documented in the licensee's CAP as PER 142319. This finding was of very low safety significance because there was no substantial potential for overexposure and the licensee's ability to assess dose was not compromised.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

W. Baker, Operations Unit Supervisor
S. Berry, Systems Engineering Manager
S. Bono, Director of Engineering
M. Button, Maintenance Manager
S. Cephus, Component Engineering Supervisor
P. Chadwell, Operations Manager
J. Emens, Site Licensing Supervisor
D. Feldman, Operations Support Superintendent
A. Feltman, Emergency Preparedness Manager
E. Frevold, Design Engineering Manager
R. Glisson, Maintenance Support Manager
F. Godwin, Licensing Manager
D. Grissette, Director of Site Technical Support
L. Hughes, Operations Superintendent
J. McCarthy, Director of Safety and Licensing
M. McLaughlin, Unit Supervisor
J. Mitchell, Site Security Manager
M. Palmer, Assistant Plant Manager
R. Perry, Fire Protection Shift Supervisor
B. Pierce, Chemistry/Environmental Manager
B. Quinn, Daily Scheduling Manager
E. Quinn, Performance Improvement Manager
J. Randich, General Manager of Operations
R. Rogers, Modifications and Projects Manager
P. Sawyer, Radiation Protection Manager
J. Underwood, Site Nuclear Assurance Manager
J. Walton, Radiation Protection Supervisor
R. West, Site Vice President

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Opened

05000259, 260, 296/2009003-04 URI Inadequate Scoping of Risk Significant Systems For Online Risk Assessment (Section 4OA2.3)

Opened and Closed

05000260/2009003-01 NCV Failure to Assess and Manage Shutdown Risk Associated with Outage Maintenance Activities (Section 1R13)
05000259/2009003-02 NCV Failure to Perform an Adequate Risk Assessment during Severe Weather Conditions (Section 1R13)
05000259, 260, 296/2009003-03 NCV Failure to Comply with the Requirements of an RWP by Entering a Posted High Radiation Area (Section 2OS1)
05000259/2009003-05 FIN Untimely Actions to Resolve Excessive IBC System Condensation Results in Unit 1 Reactor Scram

(Section 4OA3.2)

Closed

LER
05000260/2009001-00
LER Manual Reactor Scram Following Stator Cooling Water Equipment Failure (Section 4OA3.1)
LER
05000259/LER-2009-001-00 LER Turbine Trip and Reactor Scram Due to Power Load Unbalance Signal on the Main Generator

(Section 4OA3.2)

LER
05000259/LER-2009-002-00 LER Unexpected Logic Lockout of the Loop II Residual Heat Removal System Pumps (Section 4OA3.3)

Discussed

None

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

0-GOI-200-3, Hot Weather Operations, rev. 9
IGA-6, Power System Operations, Rev. 11
SPP-7.1, On-Line Work management, Rev. 13 0-GOI-300-4, Switchyard Manual, Rev. 74
NOM-SDP-7-SYR-Work Plan, Work Plan and Development and Performance for Switchyard Risk Activities, Rev. 4
TRO-VP-SPP-10.006, Loss of SCADA and/or EMS, Rev. 3
TRO-TO-SOP-10.128, Browns Ferry Nuclear Plant (BFN) Grid Operating Guide
TRO-TO-SOP-10.328, Nuclear Offsite Disqualification Notification and Call-Out Procedure, Rev.

Section 1R04: Equipment Alignment

2-OI-75 Attachment 1, Core Spray System Valve Lineup Checklist, March 19, 2007 2-OI-75 Attachment 2, Core Spray System Panel Lineup Checklist, March 19, 2007
2-OI-75 Attachment 3, Core Spray System Electrical Lineup Checklist, March 19, 2007 Drawing 3-47E812-1, Flow Diagram High Pressure Coolant Injection System 3-OI-74, Residual Heat Removal System, Rev. 86
3-OI-74, Attachment 1, RHR System Valve Lineup Checklist, Rev. 86
3-OI-74, Attachment 2, RHR System Panel Lineup Checklist, Rev. 86 3-OI-74, Attachment 3, RHR System Electrical Lineup Checklist, Rev. 86 Drawing 3-47E811-1, Flow Diagram Residual Heat Removal System, Rev. 64

Section 1R05: Fire Protection

Fire Protection Report, Volume 1, Section 2 Fire Hazards Analysis, Rev. 4 Fire Protection Report, Volume 2, Section
IV.3, Pre-Plan No.
RX1-621, Rev. 8
Fire Protection Report, Volume 2, Section
IV.6, Pre-Plan No.
RX2-639, Rev. 8 Fire Protection Report, Volume 2, Section
IV.9, Pre-Plan No.
RX3-593, Rev. 8 Fire Protection Report, Volume 2, Section
IV.9, Pre-Plan No.
RX3-621, Rev. 8 Fire Protection Report, Volume 2, Section
IV.9, Pre-Plan No.
RX3-639, Rev. 8 Fire Protection Report, Volume 2, Section
IV.11, Pre-Plan No.
CB2-593, Rev. 8
Fire Protection Impairment 08-1840, Door 651 Fire Protection Impairment 09-1898, Scaffold Fire Protection Impairment 09-1920, Hourly Roving Watch SSI Manual Actions Fire Protection Impairment 09-1935, B3 EECW Pump Tagged Out Fire Protection Impairment 09-1819, Unit 2 Outage Scaffolding Fire Protection Impairment 09-1920, Hourly Roving Watch SSI Manual Actions Fire Protection Impairment 09-1939, A3 EECW Pump Tagged Out Fire Protection Impairment 09-1935, B3 EECW Pump Tagged Out 0-SI-4.11.G.1.b(4), Visual Inspection of Fourth Period Appendix R Fire Dampers, Rev. 11
0-SI-4.11.G.1.b(5), Visual Inspection of Fifth Period Appendix R Fire Dampers, Rev. 5 Drawing 3-47E3392-627, Fire Protection 10CFR50 Appendix R Penetration Seal Tabular Drawing
EL 621.25 Details J, L, M, N, P & Q, Rev. 4
Attachment Drawing 0-47W391-2, Fire Protection 10CFR50 Appendix R Penetration Seal Typical Details Flexible Fire Seals
FB-1, -1A, -2, & -3, Rev. 0

Section 1R08: Inservice Inspection

Corrective Action Documents
PER 163525, EPU Steam Dryer Analysis - T Beam, 02/12/2009
PER 166823, Engineering Function Evaluation of the Reactor Cavity Head for Unit 2, 03/25/2009
PER 147298, 2-FCV-64-31 Closure Stroke Time, 06/25/2008
PER 152782, Linear Indications, 09/18/2008
PER 141734, 2A RHRSW Inlet Header Pinhole Leak, 04/07/2008
PER 146170, Steam Leak on 2-FCV-001-00146, 06/01/2008
PER 121787, Indication in N9 Nozzle to Vessel Weld, 03/17/2007
PER 121003, NOI U2C14-017, CRD Weld Indication, 03/06/2007
PER 169585, RHRSW Effluent, 04/26/2009

Procedures

N-VT-1, Rev. 44, Visual Examination Procedure for ASME Section Xi Preservice and Inservice, 04/21/2009 N-PT-9, Rev. 33, Liquid Penetrant Examination of ASME and ANSI Code Components and Welds, 02/18/2009 N-UT-78, Rev. 5, PDI Generic Procedure for the Manual Ultrasonic Examination of Reactor Pressure Vessel Welds
PDI-UT-6, 08/11/2008 N-UT-79, Rev. 2, PDI Generic Procedure for the Manual Ultrasonic Through Wall and Length Sizing of Ultrasonic Indications in Reactor Pressure Vessel Welds
PDI-UT-7, 08/18/2008 N-UT-84, Rev. 0, Procedure for the Phased Array Ultrasonic Examination of Austenitic and Ferritic Pipe Welds, 10/21/2008 54-ISI-363, Rev. 5, Remote Underwater In-Vessel Visual Inspection of Reactor Pressure Vessel Internals, Components, and Associated Repairs in Boiling Water Reactors, 10/21/2008

Other Documents

CRP-ENG-SS-08-005, Snapshot Self-Assessment Report, 04/30/08 Corporate Engineering Welding Assessment Report, 08/03/2004 Browns Ferry Nuclear Plant (BFN) - Unit 2 - American Society of Mechanical Engineers (ASME)Section XI, Inservice Inspection, System Pressure Test, Containment Inspection (IWE), and Repair and Replacement Programs - Summary Reports (NIS-1 and
NIS-2) for Cycle 14 Operation, 07/16/2007 2-SI-4.6.G Rev 36, Inservice Inspection and Risk-Informed Inservice Inspection Program Unit 2, 04/10/2009 ISI Report# R117, RPV Nozzle Ultrasonic Examination Summary Sheet Report# R074, Examination Summary and Resolution Data Sheet
MDQ206820070013 Rev 0, N-9 Nozzle Weld Flaw Evaluation per
IWB-3600
WCAP-16845-NP Rev 0, Metallurgical Investigation of Recorded Indications at the Check Valve to Pipe Dissimilar Metal Weld at Browns Ferry Unit 2 Nuclear Generating Station Digital Thermometer Calibration Sheet, Calibration No.
522350, 08/16/2008 Digital Thermometer Calibration Sheet, Calibration No.
558272, 06/20/2008
Light Meter Calibration Sheet, Calibration No. E31629, 06/18/2008 Report No. R041, Record of Liquid Penetrant Exam Report No. R049, Examination Summary and Resolution Sheet Certified Test Report, Spotcheck Developer
SKD-S2, Batch 05A10K, 02/01/2005
Attachment Certified Test Report, Spotcheck Cleaner/Remover
SKC-S, Batch 07A06K, 01/30/2007 Certified Test Report, Spotcheck Penetrant
SKL-SP1, Batch 05G02K, 07/15/2005 Certified Test Report, Ultragel II Batch 06125, 04/18/2006 Certification of Test, Calibration Block
WB-78, 03/27/2002 Certificate of Calibration, Phasor XS Flaw Detector, Serial No. E41820, 08/06/2008 Certification of Conformity, Probe 01XC90, 03/18/2009
WO# 09-711929-000, Replace Valve
BFR-1-SHV-067-0655 WPQR GT11-SPEC-1, Procedure Qualification Record, 12/29/1987 WPQR GT11-0-1A, Procedure Qualification Record, 01/26/1981 WPQR GTA18-B-1, Procedure Qualification Record, 03/01/2004

Section 1R11: Licensed Operator Requalification Program

OPDP-1, Conduct of Operations, Rev. 9 OPL173S280, Simulator Evaluation Guide, Group 6 Isolation and Main Steam Line Break in Containment, Rev. 1 2-AOI-64-2D, Group 6 Ventilation System Isolation, Rev. 30 2-EOI-1 Flowchart, RPV Control, Rev. 12 2-EOI-2 Flowchart, Primary Containment Control, Rev. 10

Section 1R12: Maintenance Effectiveness

SPP-6.6, Maintenance Rule Performance Indicator Monitoring, Trending and Reporting - 10CFR50.65, Rev. 9 0-TI-346, Maintenance Rule Performance Indicator Monitoring, Trending and Reporting - 10CFR50.65, Rev. 34
PER 160047, Unplanned LCO Entry due to Ground on HPCI Logic
PER 160537, HPCI Declared Inoperable Following Testing of 2-FCV-73-16
PER 152914, Maintenance Rule (a)(1) Status for Unit 2 HPCI
PER 144253, Unit 2 HPCI Oil Sample High Moisture
PER 137060, Unit 2 HPCI Steam Admission Valve Wedge Binding
PER 137859, U2 HPCI Steam Admission Valve Pressure Seal Ring Failure
PER 137687, Wrong Parts used for U2 HPCI Steam Admission Valve Repair Unit 2 Function 073-B (a)(1) Plan, Rev. 0
CDE 663, 2-FCV-073-0016 Extended Maintenance for Seat Leakage
CDE 690, 2-PMP-073-0054 Extended Maintenance for Water Intrusion in Oil MREP Meeting Minutes dated 3/13/2008 MREP Meeting Minutes dated 9/11/2008
MCI-0-000-GTV002, Double Disc, Pressure Seal Gate Valves, Rev. 2
PER 162961, Unit 1 RCIC in Maintenance Rule (a)(1) Status
PER 158304, U1 RCIC Governor Valve Failed to Re-open Following Flow Test
PER 158928, 1-FCV-71-3, RCIC Outboard Steam Supply Valve Failed to Open During Testing Unit 1 Function 071-B (a)(1) Plan, Rev. 0
CDE 729, 1-FCV-071-0010 Binding
CDE 730, 1-FCV-71-3 Fails to Open MREP Meeting Minutes dated 3/19/2009
MPI-0-071-TRB001, Reactor Core Isolation Cooling (RCIC) Turbine Preventative Maintenance, Rev. 24
Attachment

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

0-TI-367, BFN Equipment to Plant Risk Matrix, Rev. 10
BP-336, Risk Determination and Risk Management, Rev. 7
SPP-7.1, On Line Work Management, Rev. 12
SPP-7.2, Outage Management, Rev. 13
SPP-7.3, Work Activity Risk Management Process, Rev. 0
PER 168316, Sentinel Program Not Posted Browns Ferry Plan of the Day Dated April 9, 2009 Sentinel Runs Dated April 6-9, 2009 Browns Ferry Plant 12 Week Rolling Schedule T-0 Summary for
WW 2915
BP-336 Plant Protected Equipment report (4/21 and 4/22/09) Unit 2 Sentinel reports (4/21 and 4/22/09) T-0 Summary Report for Work Week #2917
PER 169448, Contingency Actions Not Performed in a Timely Manner for OOS Risk Sig Equip
BP-336 Plant Protected Equipment report (5/4/09) Unit 2 Sentinel reports (5/4/09) Unit 1 Daily Plant Status Report (5/4/09) T-0 Summary Report for Work Week #2919
PRA Evaluation Response -
BFN-0-09-029
PER 170184, Installation of N-1 Nozzle
PER 170184, Diesel Removed From Service During Severe Weather
ORAM Reports (5/19 and 5/20/09)
Unit 2 Outage Reports (5/19 and 5/20/09)
BP-336 Protected Equipment Log ORAM Logic Database Report for Shutdown Cooling Unit 2 Decay Heat Removal Decay Curves
PER 171728, Unplanned Entry into ORAM Orange Condition due to B Secondary ADHR Pump Failure

Section 1R15: Operability Evaluations

PER 169397, Flow Error in
FE 43292
PER 167344, EECW Low Flow to 2B Core Spray Room Cooler 0-TI-54, EECW System Operational Flush, Rev. 9
2-SI-3.2.4, EECW Check Valve Test, Rev. 39 General Design Criteria
BFN-50-7075, Core Spray Cooling System, Rev. 11 General Design Criteria
BFN-50-7067, Emergency Equipment Cooling Water System, Rev. 17 General Design Criteria
BFN-50-7064B, Reactor Building Ventilation System, Rev. 11 Calculation
MD-Q0067-930043, RHR and Core Spray Room Cooler Analysis, Rev. 6 Calculation
MD-Q0067-2005-0027, Flow Element Constants for EECW Flow Elements, Rev. 0 Drawing 2-47E859-1, Emergency Equipment Cooling Water System Flow Diagram, Rev. 29 FSAR Section 10.10, Emergency Equipment Cooling Water System,
BFN 22 Technical Specifications and Bases 3.7.2, Emergency Equipment Cooling Water and Ultimate Heat Sink, Amendment 255
PER 163879, 0-SR-3.8.1.8(I) Acceptance Criteria Step Not Satisfied Attachment
PER 164013, Unit 1 Main Turbine TGOP Drawing and Wiring Discrepancies
PER 164083, 480V Load Shed Reportability Determination
PER 166870, FE on TGOP Past Operability Drawing 0-45E602-5, Wiring Diagram Turbo-Generator Auxiliaries Schematic Diagram, Rev. 8 Drawing
1-0124B3723, Main Turbine Gear Oil Pump Sub No. 20, Rev. 0 Drawing 1-45E1748-4, Wiring Diagram 480V Shutdown Board 1B Connection Diagram, Rev. 9
WO 09-711952-000, Troubleshoot U1 TGOP Failure to Load Shed 0-SR-3.8.1.8(I), 480V Load Shedding Logic System Functional Test (Division I), Rev. 11 Calculation EDQ005720020069, Diesel Load Study for Units 1 and 2, Rev. 13 Calculation EDQ0057920034, 4.16KV and 480V Bus Load, Voltage Drop and Short Circuit Calculation, Rev. 42 Technical Specification and Bases 3.8.1, Electrical Power Systems, AC Sources - Operating, Units 1 and 2, Amendment 249 and Revision 52 respectively FSAR, Section 8.5 Standby AC Power Supply and Distribution,
BFN 22
PER 147819, Steam Leak in 3B SJAE Room
PER 147858, Implementation of Safety Procedure 806 for 3B SJAE Room Leak
PER 147854, Potential Water Entry into 3A CBP Oil System Drawing 3-47E801-2, Flow Diagram Main Steam, Rev. 27 Drawing 3-47W405-8, Mechanical Offgas System, Rev. 6 Drawing 0-47W400-8, Mechanical Main Steam Piping, Rev. 1 Drawing 0-47W400-5, Mechanical Main Steam Piping, Rev. 3 Drawing 0-47W400-4, Mechanical Main Steam Piping, Rev. 5
WO 08-718477-001, 3B SJAE Leak Repair 3-SI-3.2.29, MSIV Alternate Leak Path Testing, Rev. 5 3-SI-3.2.30, MSIV Alternate Leak Path - Cold Shutdown Testing, Rev. 3 Calculation
MD-Q0001-000006, Cracking Pressure for Check Valves 1/2/3-BFN-CKV-001-0742 and -744, Rev. 1 Calculation
MD-Q0001-960036, MSIV Leakage Containment System Boundaries, Physical Boundaries - System 001, Rev. 4
BFN-50-7001, General Design Criteria for Main Steam System, Rev. 23 DCN T41019, Mods for MS Isolation and Seismic Ruggedness (Unit 3), Rev. A
NEDC-31858P-A, BWROG Report for Increasing MSIV Leakage Rate Limits and Elimination of Leakage Control Systems, August 1999
Unit 2 Technical Specifications Section 3.6.2.2, Suppression Pool Water Level Unit 2 Technical Specifications Section 3.3.3.2, Backup Control System
PER 169830, Compliance Instrument 1-LI-64-54B Out of Tolerance
PER 172826, Inaccurate Unit 1 Suppression Pool Level Indication at Backup Control Panel
Functional Evaluation 43376 (for
PER 169830), Loops 1-LI-64-54 and 1-LI-64-66 Do Not Track
WO 09-714949-003, Perform Flush and Troubleshoot 1-LI-64-54 and 1-LI-64-66
WO 09-714949-004, Troubleshoot Level Readings of 1-LI-64-54 and 1-LI-64-66
PER 171208, Unacceptable Coatings Degradation in Unit 2 Primary Containment
Functional Evaluation 43508 (for
PER 171208), Uncontrolled Coatings Exceed Design Limit
GEH-NE-0000-0103-0409, Increased Unqualified Coatings Assessment for Browns Ferry MDQ099920060011, Transient NPSH/Containment Pressure Evaluation of RHR and CS Pumps
UFSAR Section 5.2, Primary Containment System UFSAR Section 6.5.5, Potential Plugging of Emergency Core Cooling System Suction Strainers
Attachment

Section 1R18: Plant Modifications

DCN 69528, Replace ASCO Solenoid Valves With Similar AVCO Valves, Rev. A FSAR Section 5.3 Secondary Containment System,
BFN-22 Technical Specifications and Bases 3.6.4.1 Secondary Containment, Amendment 290 Technical Specifications and Bases 3.6.4.2 Secondary Containment Isolation Valves (SCIVs), Amendment 290 Technical Requirements Manual for Browns Ferry Nuclear Plant, Appendix A, Power Operated Secondary Containment Isolation Valves, Rev. 0 General Design Criteria Document 7064B, Reactor Building Ventilation System, Rev. 13 General Design Criteria Document 7064C, Secondary Containment, Rev. 15 General Design Criteria Document 7200B, 120 VAC Power Supply and Distribution, Rev. 11
General Design Criteria Document 7307, Post Accident Monitoring, Rev. 10 Drawing 3-47E865-12, Reactor Building Ventilation Flow Diagram, Rev. 45
PER 153130, Unit 2 Reactor Zone Fan Damper 2-FCO-64-43 Failed Open
WO 08-724013-018, Unit 3 Refuel Zone Exhaust Duct Outboard Isolation Damper ASCO Solenoid Replacement With AVCO
WO 08-724013-019, Unit 3 Refuel Zone Exhaust Duct Inboard Isolation Damper ASCO Solenoid Replacement With AVCO 0-SR-3.6.4.2.1, Secondary Containment Isolation Valve Stroke Timing, Rev. 12 EDQ2999920313, Mini-Calculation for Voltage Drop and Load Analysis for Modification on the 120v System of Unit 1 and 2, Rev. 98
PER 168128, Temporary Equipment Control Item Identified During Audit No. SSA0903
PER 173527, No Briefing Sheet Attached as Required
PER 173937, Temporary Monitoring Equipment in Noncompliance with
MMDP-1 and
SPP-9.5
PER 173939, 0-TI-230V Does Not Reference
MMDP-1 or
SPP-9.5
SPP-9.5, Temporary Alterations, Rev. 8
SPP-10.1, System Status Control, Rev. 4
TACF-1-08-010-001 Rev. 0, Temporary Installation of Vibration Monitoring Instrumentation, cables and recorder(s) on the Unit 1 Main Steam System Turbine Stop and Control Valves
  1. 1 and #4.
WO 08-711302-000, Installation of Vibration Equipment on Unit 2 RHRSW HX Outlet Valves
WO 08-715494-000, Installation of Vibration Equipment on Unit 3 RHRSW HX Outlet Valves 0-OI-23, Residual Heat Removal Service Water System, Rev. 87 0-TI-230V, Vibration Monitoring, Rev. 6
0-TI-405, Plant Modifications and Design Change Control, Rev. 0 1/2/3-OI-74, Residual Heat Removal System, Revs. 66, 144, and 86 respectively FSAR Section 10.9, RHR Service Water System,
BFN-22 Technical Specifications and Bases 3.7.1, Residual Heat Removal Service Water System (RHRSW) and Ultimate Heat Sink (UHS), Rev. 44

Section 1R19: Post-Maintenance Testing

3-SI-4.5.C.1(2), EECW Pump Operation, Rev 102
0-SI-4.5.C.1(4), EECW Annual Flow Rate Test, Rev. 40
0-SI-3.1.11, EECW Pump Baseline Data Acquisition and Evaluation, Rev. 25 0-SI-3.1.4, EECW Pump Performance, Rev. 47 0-TI-345, EECW Pump Curve Data Acquisition, Rev. 5 0-TI-362, Inservice Testing of Pumps and Valves, Rev. 22
Attachment 0-TI-383, Evaluation of Test Results for the ASME OM Code Inservice Testing Program, Rev. 1
SPP-9.1, ASME Section XI, Rev. 8
MCI-0-023-PMP002, EECW and RHRSW Pump (Byron Jackson Type KX) Disassembly, Inspection, Rework and Reassembly, Rev. 47
MCI-0-023-PMP003, EECW and RHRSW Pump (Byron Jackson Type KX) Removal and Reinstallation, Rev. 10
MCI-0-023-PMP004, EECW and RHRSW Pump Impeller Adjustment, Rev. 3
ECI-0-000-MOT001, Removal and Installation of AC and DC Motors, Rev. 54
EPI-0-000-TST001, Bridge, Megger and High Potential Testing of Electrical Equipment, Rev. 56 Work Order 08-716204-000, Replace Upper Column Shaft on A3 EECW Pump Work Order 08-716204-001, MSB Support for removal of A3 EECW Pump Motor Work Order 09-712134-000, Replace A3 EECW Pump with refurbished Pump Work Order 08-712134-001, MSB Support for removal of A3 EECW Pump Motor Work Order 09-714533-000, Adjust Impeller on A3 EECW Pump Work Order 09-715933-000, Remove A3 EECW Pump for Inspection Work Order 09-715933-001, MSB Support for removal of A3 EECW Pump Motor Work Order 09-715933-003, Support for Testing of A3 EECW Pump Evaluation 09-0-IST-023-389, Evaluation of ASME OM Code IST Test Results for A3 EECW Pump BFN Unit 3 Technical Specifications Section 3.7.2, Emergency Equipment Cooling Water System and Ultimate heat Sink BFN USFAR Section 10.10, Emergency Equipment Cooling Water System Drawing 1-47E858-1-ISI, ASME Section XI RHR Service Water System Code Class Boundaries, Rev. 24 Drawing 1-47E859-1-ISI, ASME Section XI Emergency Equipment Cooling Water System Code Class Boundaries, Rev. 76
PER 35566, Tolerance for Setting RHR and CS Pump Flow Rates During Section XI Tests Cause Total Accuracy To Exceed 2percent
PER 166464, A3 EECW Pump Has Audible Knocking Sound
PER 167222, Unplanned Unavailability on the A3 EECW Pump
PER 167411, A3 EECW Pump Strainer Basket Damaged
PER 167758, Alignment Issues on A3 EECW Pump Due To Tight Packing
PER 168420, A3 EECW Pump Failed During 3-SI-4.5.C.1(2)
PER 168967, A3 EECW Pump Repeat Failure during PMT Surveillance
PER 172453, No Correction Factor Applied for Level Drop Across the Traveling Screen During Baseline Data Acquisition
PER 174373, Baseline Testing of A3 EECW Pump Could Not Be Used Due To Not Obtaining a Data Point at Design Flow Rate.
PER 174469, 0-SI-4.5.C.1(4), EECW System Annual Flowrate Not Initially Performed After Replacement of A3 EECW Pump on 4/7/2009
PER 174835, Procedure Revision Failed to Address Question of Operability of Non-Tested Pump
PER 174914, Confusion and Inconsistency in the Use of "N/A" During Surveillances
PER 174991, 0-TI-345 Steps Performed Out-of-sequence
PER 175117, A3 EECW Pump Testing Improvements
PER 175238, No 10CFR50.59 Screening Performed for Change to EECW Surveillance Procedure
PER 175244, Improvements in Quality Needed in Procedure 0-TI-345
PER 175252, Quarterly Surveillance Results Used to Establish Baseline Flow Instead of Pump Curve Flow at the Reference Point
PER 175254, Temperature Affects Masking Pump Degradation in EECW IST Tests Attachment
PER 175255, Alert and Action Required Flows Reduced Due to Instrument Inaccuracy
WO 08-712349-000, Insert Riser Isolation Valve Packing Replacement
MCI-0-000-GTV001, General Maintenance Instructions for Gate Valves, Rev.21
MCI-0-000-PCK001, General Maintenance Instructions for Valve Packing, Rev.21
MSI-0-000-PLG001, Installation of Freeze Seals, Rev.34
OPL171.006, Licensed Certification Training for Control Rod Blade and Drive Mechanism, Rev.
Drawing 2-47E820-2, Flow Diagram Control Rod Drive Hydraulic System, Rev.14 FSAR Section 3.4, Reactivity Control Mechanical Design,
BFN-22
WO 09-711929-000, North Header Supply to Core Spray II Cooler Valve Replacement
WO 08-724315-000, Monthly Monitoring of 1B CS Room Cooler Flow 0-OI-67, Emergency Equipment Cooling Water System, Rev. 85
PER 170170, North Header Supply to NE Core Spray Room Cooler Structural Integrity
PER 170453, Div II RHR Room Cooler Vent Valve Failure
PER 170454, A3 EECW Pump Operated Below Minimum Flow
PER 170456,
OI-67 Caused A3 EECW Pump to Operate Below Minimum Flow
1-SI-3.2.4, EECW Check Valve Test, Rev. 31 Tagout 0-TO-2009-0001, Clearance 0-067-0010, 1-SHV-067-0655
Work Order 07-721562-002, Implement
DCN 69391, Stage 3 Work Order 07-721562-003, Uncouple and Couple 2D CS Pump from Motor Work Order 07-721562-005, Perform PMTs Following Replacement of 2D CS Pump Motor Work Order 07-721562-007, Perform Bridge and Megger on 2D CS Pump Motor 2-SR-3.5.1.6(CS
II-Comp), Core Spray Loop II Comprehensive Pump Test, Rev. 3
ECI-0-000-MOT001, Removal and Installation of AC and DC Motors, Rev. 54
EPI-0-000-TST001, Bridge, Megger and High Potential Testing of Electrical Equipment, Rev. 55
MCI-0-075-PMP001, Core Spray Bingham Centrifugal 12x16x14 1/2 One Stage Disassembly, Inspection, Rework and Reassembly, Rev. 8 BFN Unit 2 Technical Specifications Section 3.5.1, ECCS - Operating BFN USFAR Section 6.4.3, Core Spray System Description BFN USFAR Section 6.5.2.4, Core Spray System

WOs

07-722378-008, -012, and -014, RHRSW HX Outlet Valve Replacement/Modification
WO 09-716814-000, Vibration Testing on RHRSW HX Outlet Valve 23-52
ECI-0-000-MOV009, Testing of Motor Operated Valves Using MOVATS Universal Diagnostic System (UDS) and Viper 20, Rev. 21
MCI-0-000-PCK001, Generic Maintenance Instruction for Valve Packing, Rev. 21
MCI-0-023-VLV001, RHR Service Water Motor Operated Valves 1/2-FCV-23-34, -40, -46, and 52 Disassembly, Inspection, Rework, and Reassembly, Rev. 17
PER 171832, D2 RHRSW Pump Failed Flow Test
PER 171914, Vibration Testing Not Specified as Part of Modification Testing
PER 171929, Poor Decision to Run ASME XI Pump Test for Valve PMT
PER 172442, New Copes Vulcan Valve Stroke Limitations
2-SI-4.5.C.1(3), RHRSW Pump and Header Operability and Flow Test, Rev.103
WO 07-721570-002, Implement
DCN 69631 Stage 1, Remove/Replace RHR 2B Pump Motor (BFN-2-MTR-074-0028)
WO 07-721571-002, Implement
DCN 69631 Stage 1, Remove/Replace RHR 2D Pump Motor (BFN-2-MTR-074-0039)
Attachment
WO 07-721570-005, Implement
DCN 69631 Post-modification Testing for 2B RHR Pump Motor
WO 07-721571-005, Implement
DCN 69631 Post-modification Testing for 2D RHR Pump Motor
WO 07-721570-006, Support
DCN 69631 for Replacement of 2B RHR Pump Motor by Performing Electrical Testing
WO 07-721571-007, Support
DCN 69631 for Replacement of 2D RHR Pump Motor by Performing Electrical Testing 2-SR-3.5.1.6 (RHR
II-COMP), RHR Loop II Comprehensive Pump Test
DCN 69391 Technical Evaluation Post-Modification Testing Control Form for
DCN 69631
ECI-0-000-MOT001, Removal and Installation of AC and DC Motors
EPI-0-000-TST001, Bridge, Megger, and High Potential Testing of Electrical Equipment

Section 1R20: Refueling and Other Outage Activities

Browns Ferry Nuclear Plant Outage Risk Assessment Report Unit 2 Cycle 15 RFO Cycle 16, April 10, 2009 2-POI-200.5, Operations with Potential for Draining the Reactor Vessel/Cavity, Rev. 12 Drawing 2-47E820-2, Flow Diagram Control Rod Drive Hydraulic System, Rev. 14 2-AOI-100-1, Reactor Scram, Rev. 91 2-GOI-100-12A, Unit Shutdown from Power Operation to Cold Shutdown and Reductions in Power during Power Operations, Rev. 92 2-OI-1, Main Steam System, Rev. 45 2-GOI-100-3A, Refueling Operations (RX Vessel Disassembly and Floodup), Rev. 37 2-GOI-100-3B, Refueling Operations (Reactor Cavity Letdown and Vessel Re-Assembly), Rev.
2-SI-3.3.1.A, ASME Section XI System Leakage Test of the Reactor Vessel and Associated Piping, Rev. 25 2-SR-3.4.9.1(1), Reactor Heatup and Cooldown Rate Monitoring, Rev. 18 2-SR-3.3.2.1.2, RWM Functional Test for Startup, Rev. 3 2-SR-3.3.2.1.7, RWM Program Verification, Rev. 2 2-SR-3.1.3.5(A), Control Rod Coupling Integrity Check, Rev. 20
2-SR-3.1.3.5(B), CRD Coupling Integrity Check After Refueling or Maintenance, Rev. 4

Section 1R22: Surveillance Testing

1-SR-3.5.1.6(CS I), Quarterly CS System Flow Rate Test Loop I
WO 08-724100-000, Electrical Maintenance PM for Monitoring CS Motor Bearing and Winding Temperatures BFN Unit 1 Technical Specifications Section 3.5.1, ECCS - Operating
0-SR-3.8.1.9(D), Diesel Generator D Emergency Unit 2 Load Acceptance Test, Rev. 13 BFN Unit 1 Technical Specifications Section 3.8.1, AC Sources - Operating
BFN Unit 1 Technical Specifications Section 3.8.3, Diesel Generator Fuel Oil, Lube Oil and Starting Air BFN Unit 1 Technical Requirements Manual TRM 3.8.1, Diesel Generators BFN USFAR Section 8.5, Standby A-C Power Supply and Distribution
2-SR-3.1.4.1, Scram Insertion Times, Rev. 26 Technical Specifications and Bases 3.1.4 Control Rod Scram Times, Amendment 295 Technical Specifications and Bases 3.1.3 Control Rod Operability, Amendment 253
Attachment
PER 174698, AUO Retrieved Valve Label from Radiological Contaminated Area with Bare Hands
PER 175018,
CRD 46-23 Declared Slow
PER 175023, Evaluate Scram Insertion Time Testing on HWC Operation
2-SR-3.4.3.2, Main Steam Relief Valve Manual Cycle Test
BFN Unit 2 Technical Specifications Section 3.4.3, Safety/Relief Valves BFN Unit 2 Technical Specifications Bases Section 3.4.3, Safety/Relief Valves
PER 173480, MSRV 2-PCV-1-23 Failed to Fully Open During Manual Cycle Test
PER 173480/WO 09-718047-000, Troubleshooting Plan
2-SI-4.7.A.2.a-f, Primary Containment Integrated Leak Rate Test
ANS 56.8 - 1994, Containment System Leakage Testing Requirements
BFN Unit 2 Technical Specifications Surveillance Requirements Section 3.6.1.1.1, Primary Containment Leakage Rate Testing Program BFN Unit 2 Technical Specifications Section 5.5.12, Primary Containment Leakage Rate Testing Program Unit 2 Primary Containment Integrated Leak Rate Test Management Briefing Package
PER 172291, Numerous Problems and Delays Encountered During Setup for CILRT Pressurization

Section 1EP6: Drill Evaluation

Emergency Plan Implementation Procedure (EPIP) 1, Emergency Classification Procedure, Rev. 43 EPIP 3, Alert, Rev. 32
EPIP 4, Site Area Emergency, Rev. 31 Performance Indicator Data, 2009 BFN Blue Team Training Drill, 4/07/2009

Section 2OS1: Access Control to Radiologically Significant Areas

Procedures, Guidance Documents, and Manuals
SPP-5.1, Radiological Controls, Rev. 6
RCDP-7, Bioassay and Internal Dose Program, Rev. 1
RCTP-106, Special Dosimetry Operations, Rev. 1
RCI-8.1, Internal Dosimetry Program Implementation, Rev. 41
RCI-9.1, Radiation Work Permits, Rev. 57
RCI-17, Control of High Radiation Areas and Very High Radiation Areas, Rev. 65
RCI-31,
HI-STORM Five Year Shielding Effectiveness Surveys, Rev. 0
RCI-33, Underwater Diving Operations, Rev. 7
RCI-40.3, RP Actions for Operation's Unit 3 Procedural Hold Points, Rev. 8
RCI-41, Radiation Protection's Periodic Routines, Rev. 2
Records and Data Whole Body Count Results and Internal Dose Assessment, May 1-6, 2009
Dosimetry Investigation Report 08-093 Radiological Incident Reports:
20080044,
20090011 SDE/DDE/LDE Calculation,
PC 20090011
Radiation Work Permits
Attachment
08330061, Unit 3 Maintenance on Heater Vents/Drains (Various Dress)
08372135, U3C13 Laundry/Trash Pickup/Labcoat Dressout
08380028, U3C13 DW Radcon Support (LHRA, Resp, Various Dress)
08382236, U3C13 DW Cut-out Replace 73-2 (LHRA Various Dress)
09270045, U2C15 Rx Bldg Scaffold Support (High Rad/Various Dress)
09270081, U2C15 Rx Bldg Movats (Various Dress)
280025, U2C15 Drywell Radcon Outage Support (Dose Control/High Rad/Various Dress)
09280095, U2C15 DW ISI, IWE, Fac (High Rad/Various Dress)
09290018, U2C15 Refuel Floor Steam Dryer Tie Bar Repair (LHRA, Extremity & Multibadging)
Radiation Surveys
051209-32, Unit 2 Drywell 628'
051209-31, Unit 2 Drywell 616'
051209-29, Unit 2 Drywell 604'
051109-36, Unit 2 Drywell 584'
051209-20, Unit 2 Drywell 563'
042809-61, Unit 2 Drywell 550'
050409-12, Unit 2 Drywell 550'
043009-10, Unit 2
RXB 519' SE Quad
051409-40, Unit 2
RXB 519' SE Quad 051709-1, Unit 2
RXB 519' SE Quad 041508-9, Unit 3
RXB 565' General Area 041408-5, Unit 3 Drywell 550'
040308-30, Unit 3
RXB 519' Under Torus
051808-25, Unit 3
TB 586' 3B SJAE Room
052008-26, Unit 3
TB 586' 3B SJAE Room 020409-1, Unit 3
RXB 519' SE Quad
020609-16, Unit 3
RXB 519' SE Quad
21609-32, Unit 3
RXB 519' SE Quad
050809-16, Low Level Module Warehouse
050709-24, Low Level Modules 032509-1, ISFSI Pad
033109-18, ISFSI Pad
040709-19, ISFSI Pad
042809-71, ISFSI Pad 050609-3, ISFSI Pad 050609-1, ISFSI Pad 051309-3, ISFSI Pad
CAP Documents
BFN-RP-F-09-002, Self-Assessment - High Radiation Controls, March 2009
BFN-RP-F-09-001, Self-Assessment, RP Records and Risk Management, Feb 2009
PER 141446, Dose rate alarm
PER 142410, Inadequate high radiation area barrier
PER 142604, Internal contamination
PER 145551, 3B SJAE dose rate alarm
PER 148686, Radiation Protection Program and Standards Plan
PER 150294, Great grand master key B locked high rad area keys
PER 150836, Dosimetry investigation reports08-198, 08-199, and 08-200
PER 160157, Potential negative trend in rad barrier violations
PER 164597, HRA boundary violation Attachment
PER 170118, Personnel contamination
PER 171182, Positive WBC
PER 171375, Unanticipated dose rate alarm/HRA event

Section 2OS2: As Low As Reasonably Achievable (ALARA)

Procedures, Manuals, and Guidance Documents
RCI-1.1, Radiation Operations Program Implementation, Rev. 136
RCI-15.1, Maintaining Occupational Radiation Exposures As Low As Reasonably Achievable (ALARA), Rev. 42
RCI-15.3, Radiological Safety Committee, Rev. 25
RCI-26, Radiation Protection Department Standards and Expectations, Rev. 16
RCI-27, Source Term Reduction and Control, Rev.
6
RCI-9.1, Radiation Work Permits, Revision 61
SPP-5.1, Radiological Controls Rev. 6
SPP-5.2, ALARA Program Rev. 3
SPP-7.0, Work Management, Rev. 1
SPP-7.1, On Line Work Management, Rev. 12
SPP-7.2, Outage Management, Rev. 12
Records and Data Reviewed Fiscal Year 2008 Annual ALARA Report Outage Report: BFN Unit 1 Cycle 8- February 2009 Forced Outage Declared Pregnant Women Dosimetry Documentation for 4 Women Browns Ferry Nuclear Power Plant Long-Term Collective Radiation Exposure Reduction Plan 2007 - 2011
APR 08-0005, Unit 1 Reactor Building 664' Elevation Refuel Floor, Rev.0
APR 08-0107, U1C7 Outage - Modifications To Steam Dryer To Support EPU Conditions, Rev.
APR 08-0110, U1C7 Outage - Scaffolding Support, Rev.0
APR 08-0111, U1C7 Outage - Insulation & Shielding - Remove, Maintain & Install, Rev. 0
APR 08-0124,
U1C7 Outage - 1N11B Feedwater Sensing Line Leak Repair Post Job Reviews for
APR 08-0105,
APR 08-0107,
APR 08-110,
APR 08-111 and
APR 08-124
APR 09-0041, U2C15 Outage - Refuel Floor Activities
APR 09-0042, U2C15 Outage - Scaffolding Support
APR 09-0045, U2C15 Outage - ISI, IWE, FAC & Engineering Support
APR 09-0047, U2C15 Outage - Undervessel Work Activities
APR 09-0072, U2C15 Outage - Insulation & Shielding Remove Maintain & Install Work In-Progress reviews for
APR 09-0031,
APR 09-0037,
APR 09-0045 and
APR 09-0049
TSR 07-0037, Hot spots in the Unit 2 East and West Scram Discharge Volume Cages
TSR 09-0002, U2C15 Outage Torus Snubber Bay 8 &11
TSR 09-0003, Unit 2 Reactor Building 664' elevation, Refuel Floor, R-9 and S-Line South of the
SFSP
TSR 09-0004, U2C15 Outage Drywell "Appendix A"
TSR 09-0006, U2C15 Outage In-Vessel Inspection Platform
TSR 09-0007, Unit 2 "B" & "D" RHR HEX Inlet Piping and "B & D" RHR HEX Bottom Head Internal area
TSR 09-0009, Unit 2 SE Quad 519' And 541' Crosstie Piping
TSR 09-0010, U2C15 U-2 RXB O/S Clean Room SE Corner, 565' At Column R-11/R-12 and Between T and U- Lines
TSR 09-0011, Unit 2
RXB 565' R-12 U-Line RHR Vent Line Attachment
TSR 09-0012, U2C15 Outage Drywell Activities
TSR 09-0013, U2C15 Unit 2 Drywell, 563' elevation, A,B,C & D Main steam line in support MSIV maintenance
TSR 09-0014, Unit 2
FCV-2-69-2
TSR 09-0022, Unit 0 Refuel Floor Overhead Crane
TSR 09-0024, U2C15 U-2
RXB 565' R-14/R Line (RHR Control Point)
TSR 09-0025, U2C15 "D" MSIV in the U2 Steam Tunnel
TSR 09-0034, U2C15 Junction of 3" and 4" Demin 2B Precoat Inlet Line (Photo attached)
TSR 09-0048, U2C15 FPC Valves 2-DRV-078-559 & 560
CAP Documents Fiscal Year 2008 Annual ALARA Report Outage Report: BFN Unit 1 Cycle 8- February 2009 Forced Outage Browns Ferry Nuclear Power Plant Long-Term Collective Radiation Exposure Reduction Plan 2007 - 2011
PER 153752 Documenting Source Term Reduction Efforts Being Deferred
PER 158071 UT Couplant for Encapsulating Contamination (OE)
PER 158076 Using Ultrasonic Transducers While Flushing Hot Spots
PER 159197 Overestimated Doserate By a Factor of Four (4)

Section 2PS1: Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems

Procedures, Manuals, and Guides
SPP-5.14, Guide for Communicating Inadvertent Radiological Spills/Leaks to Outside Agencies, Rev. 2
SPP-5.15, Fleet Ground Water Protection Program, Rev. 0
CI-421, Well Sampling and Maintenance, Rev. 0
Reports Annual Radiological Environmental Operating Report, 2008
CRP-TPR-S-009-003, Self-Assessment,
NEI 07-07 Groundwater Protection Initiative Compliance, December 2008

Section 2PS2: Radioactive Material Processing and Transportation

Procedures, Manuals, and Guides
0-OI-77A, Waste Collector/Surge System Processing, Rev. 57
0-OI-77B, Floor Drain Collector System Processing, Rev. 57 0-OI-77C, Radwaste Filter and Demineralizer System, Rev. 39
0-OI-77D, Backwash Receivers and Phase Separators System, Rev. 34 0-OI-77E, Solid Radwaste, Rev. 41 0-OI-77F, Thermex Operation, Rev. 20 0-OI-77G, Duratek Procedure
FO-OP-32, Set Up and Operating Procedure for the
RDS-1000 Unit at TVA Browns Ferry, Rev. 1 0-SI-4.8.F.1, Spent Resin Dewatering Process Control Verification, Rev. 18 Browns Ferry Nuclear Plant Process Control Program Manual (PCP), Rev. 3 Radioactive Material Shipment Manual (RMSM), Volume I - Information, Rev. 38
RCI-1.1, Radiation Operations Program Implementation, Rev. 130
RCI-1.2, Radiation, Contamination and Airborne Surveys, Rev. 7
RCI-15.3, Radiological Safety Committee, Rev. 25
Attachment
RCI-43, Radioactive Material Control, Rev. 0 RMSM, Volume II - Radioactive Material Shipment, Rev. 38 RMSM, Volume III - Radwaste Shipment, Rev. 38
RWTP-100, Radioactive Material/Waste Shipments, Rev. 5
RWTP-101, 10
CFR 61 Characterization, Rev. 1
RWTP-102, Use of Casks, Rev. 1
SPP 3.1, Corrective Action Program, Rev. 15
SPP-5.1, Radiological Controls, Rev. 6
Shipping Records and Radwaste Data
CFR Part 61 Reports of Analysis/Certificates of Conformance, 09/28/07 and 02/02/09
Browns Ferry Nuclear Plant (BFN) - Personnel Qualified to Ship Radioactive Material/Waste Letter to File, March 3, 2009 BFN - Units 1, 2, and 3 - Annual Radioactive Effluent Release (ARER) Reports - January through December for 2007 and 2008 Cask Book for Model CNS 8-120B, Rev. 30 Safety Analysis Report 14-195H Shipping Cask, Rev. 2 Shipment No.
080106, Cask of Dewatered Resin, 01/17/08
Shipment No.
080320, Box Containing GE Equipment, 03/31/08 Shipment No.
080435, Box Containing MSRV Main Body to Wyle Labs, 04/30/08 Shipment No.
081210, Drum Containing10
CFR 61 Samples, 12/29/08 Shipment No.
080320, Box Containing GE Equipment, 03/31/08 Shipment No.
090511, Cask of Dewatered Condensate Resin, 05/13/09
Shipment No.
090519, Sealand of Plant Waste, 05/20/09 Shipment No.
090520, Sealand of Plant Waste, 05/20/09 Shipment No.
090521, Sealand of Contaminated Plant Protective Clothing, 05/20/09
CAP Documents
PER 138682, Yellow radioactive material trash was inadvertently loaded and positioned near the bottom of a Sealand with contact dose rate reading of 400 mr/hr
PER 146000, Accident involving radioactive material shipment
PER 148447, During a safety walkdown in the Radwaste Building, two drums of spent resin appeared to be pressurized
PER 156054, This PER was initiated to ensure Effectiveness Reviews required by
PER 128870 are documented as stated in the actions TVA Nuclear Assurance - Nuclear Power Group (NPG) Wide - Radiological Protection and Control Programs - Audit Report No. SSA0702, February 15, 2008

Section 4OA1: Performance Indicator Verification

Browns Ferry Units 1/2/3 Mitigating Systems Performance Indicator MS05 through Q1/2009
SPP-3.4, Performance Indicator and MOR Submittal Using INPO Consolidated Data Entry, Rev.
NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Rev. 5 NUREG 1022, Event Reporting Guidelines 10CFR 50.72 and 50.73, Rev. 2
LER 05000296/2007-004, Manual Isolation of High Pressure Core Injection due to Steam Leak
LER 05000296/2007-005, Automatic Reactor Scram Due to Main Generator Load Reject
LER 05000259/2008001, Loss of Safety Function Reactor Zone Exhaust Dampers Failed to Close
LER 50-259/2008-002 and
LER 50-259/2008-002-01, ASME Code Class 1 Pressure Boundary Leak on an Instrument Line Connected to the Reactor Vessel Attachment
LER 50-259/2008-003, Main Steam Relief Valve As-Found Setpoint Exceeded Technical Specification Lift Pressure
LER 05000260/2008-001, Automatic Turbine and Reactor Trip Resulting From a Failure of the Design Change Process
LER 05000296/2008-001, Unanticipated Auto-Start of Emergency Diesel Generators
LER 05000296/2008-002, Main Steam Relief Valve As Found Setpoint Exceeded Technical Specification Lift Pressure Performance Indicator FAQs 128 and 422 regarding reporting date for SSFF PI.
O-SI-4.8.A.5-1, Appendix I Dose Calculations-Liquid Effluents
CI-138, Reporting NEI Indicators
O-SI-4.8.B.3, Appendix I Dose Calculations - Airborne Effluents Radiological Impact Assessment Report, January 2008-December 2008 Select Dosimetry Incident Reports involving dose rate alarms exceeding 1 rem/hr Semi-Annual Radioactive Effluent Release Report 2 (1

st Quarter 2009)

Batch Liquid Effluent Permit (March 14, 2009)
Gaseous Radioactive Waste Release Permit (March 18, 2009)
PER 142319,
WRM-2 unit LHRA electronic dosimeter retrieval

Section 4OA2: Identification and Resolution of Problems

SPP-3.1, Corrective Action Program, Rev. 14
PIDP-11, PER Trending, Rev. 2
PIDP-12, Integrated Trend Review, Rev. 1 Browns Ferry Nuclear Plant Integrated Trend Report (ITR) for January to March 2009
PER 155895, Multiple Risk Communication Errors Over Course of Days
PER 156229, Inaccurate Unit 2 Risk Condition Communicated for 4KV SD BD C
PER 157170, 1B CRD Pump and 161KV Grid Status Risk Information Inaccurate
PER 159157, POD Risk Status Page Not Updated Accurately
PER 160093, Lack of Protected Equipment Postings for Unit 2 HPCI OOS
PER 160566, Trend PER on Plant Risk
PER 160698, Mode Transition from Mode 4/5 to 3 Without Changing from ORAM to Sentinel
PER 163604,
SPP-7.1 Delays in Issuance
PER 167965, Communication of Plant Risk
PER 169790,
SPP-7.1 and 7.3 Lack of Change Management
PER 169925, EOOS (CAFTA Model) Coverage Gap
PER 170012,
SPP-7.3 Lack of Change Management and Communications
SPP-7.1, On Line Work Management, Rev. 13
SPP-7.3, Work Activity Risk Management Process, Rev. 0
BP-336, Risk Determination and Risk Management, Rev. 7 OPL171.048, Hot License Training, Raw Cooling Water, Rev. 8

Section 4OA3: Event Follow-up

1-SR-3.3.5.1.6(CS I), Core Spray System Logic Functional Test Loop I, Rev. 4 BFN Unit 1 Technical Specifications Section 3.3.5.1, ECCS Instrumentation BFN Unit 1 Technical Specifications Section 3.5.1, ECCS - Operating BFN USFAR Section 6.4.3, Core Spray System BFN USFAR Section 7.4, Emergency Core Cooling Control and Instrumentation
PER 166487, Unplanned Entry into TS 3.0.3
Attachment
PER 163815, Unit 1 Generator Trip from Isophase Bus Ground
PER 163815 Root Cause Analysis Report
PER 158940, Unit 1 Bus Duct Cooling Excessive Moisture
PER 163680, Unit 2 Reactor Scram - Stator Coil Temp Hi
PER 163680 Root Cause Analysis Report

LIST OF ACRONYMS

ADAMS Agencywide Document Access and Management System
ARM area radiation monitor
CAD containment air dilution
CAP corrective action program
CCW condenser circulating water

CFR Code of Federal Regulations

CoC certificate of compliance

CRD control rod drive
CS core spray
DCN design change notice
EECW emergency equipment cooling water
EDG emergency diesel generator
FE functional evaluation
FPR Fire Protection Report
FSAR Final Safety Analysis Report
IMC Inspection Manual Chapter
LER licensee event report
NCV non-cited violation
NRC [[]]
U.S. Nuclear Regulatory Commission
ODCM Off-Site Dose Calculation Manual
PER problem evaluation report
PCIV primary containment isolation valve
PI performance indicator
RCE Root Cause Evaluation
RCW Raw Cooling Water
RG Regulatory Guide
RHR residual heat removal
RHRSW residual heat removal service water
RTP rated thermal power
RPS reactor protection system
RWP radiation work permit
SDP significance determination process
SBGT standby gas treatment
SLC standby liquid control
SNM special nuclear material
SRV safety relief valve
SSC structure, system, or component
TI Temporary Instruction
TIP transverse in-core probe
TRM Technical Requirements Manual
TS Technical Specification(s)
UFSAR Updated Final Safety Analysis Report
URI unresolved item
WO work order