LER-2009-001, Regarding Manual Reactor Scram Following Stator Cooling Water Equipment Failure |
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| Report date: |
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| Reporting criterion: |
10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(iv)(B), System Actuation
10 CFR 50.73(a)(2)(i)
10 CFR 50.73(a)(2)(vii), Common Cause Inoperability
10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded
10 CFR 50.73(a)(2)(viii)(A)
10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition
10 CFR 50.73(a)(2)(viii)(B)
10 CFR 50.73(a)(2)(iii)
10 CFR 50.73(a)(2)(ix)(A)
10 CFR 50.73(a)(2)(x)
10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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| 2602009001R00 - NRC Website |
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Tennessee Valley Authority, Post Office Box 2000, Decatur, Alabama 35609-2000 April 20, 2009 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Mail Stop: OWFN, P1-35 Washington, D. C. 20555-0001 10 CFR 50.73
Dear Sir:
TENNESSEE VALLEY AUTHORITY - BROWNS FERRY NUCLEAR PLANT (BFN) - UNIT 2 -
DOCKET 50-260 - FACILITY OPERATING LICENSE DPR LICENSEE EVENT REPORT (LER) 50-26012009-001 -00 The enclosed report provides details of a manual reactor scram following stator cooling water equipment failure. TVA is reporting this in accordance with 10 CFR 50.73(a)(2)(iv)(A), as an event that resulted in a manual or automatic actuation of the systems listed in paragraph 10 CFR 50.73(a)(2)(iv)(B) (i.e., Reactor Protection System including reactor scram or trip, and general containment isolation signals affecting containment isolation valves in more than one system).
There are no commitments contained in this letter.
Sincerely, GWest i
President, BEN cc: See page 2
U.S. Nuclear Regulatory Commission Page 2 April 20, 2009 Enclosure cc (Enclosure):
Ms. Eva A. Brown, Project Manager U.S. Nuclear Regulatory Commission (MS 08G9)
One White Flint, North 11555 Rockville Pike Rockville, Maryland 20852-2739 Ms. Heather J. Gepford, Acting Branch Chief U.S. Nuclear Regulatory Commission Region II Sam Nunn Atlanta Federal Center 61 Forsyth Street, SW, Suite 23T85 Atlanta, Georgia 30303-8931 NRC Resident Inspector Browns Ferry Nuclear Plant 10833 Shaw Road Athens, Alabama 35611-6970
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES 08/31/2010 (9-2007)
, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
- 3. PAGE Browns Ferry Unit 2 05000260 1 of 5
- 4. TITLE: Manual Reactor Scram Following Stator Cooling Water Equipment Failure
- 5. EVENT DATE
- 6. LER NUMBER
- 7. REPORT DATE
- 8. OTHER FACILITIES INVOLVED SEQUENTIAL REV MONTH DAY YEAR FACILITY NAME DOCKET NUMBER MO YEAR YEAR NUMBER NO.
None N/A FACILITY NAME DOCKET NUMBER 001
- - e N/A
- 9. OPERATING MODE
- 11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply)
El 20.2201(b) 0l 20.2203(a)(3)(i) 0l 50.73(a)(2)(i)(C)
[I 50.73(a)(2)(vii) ol 20.2201(d)
El 20.2203(a)(3)(ii) 0l 50.73(a)(2)(ii)(A)
[: 50.73(a)(2)(viii)(A) 0l 20.2203(a)(1) 0l 20.2203(a)(4) 0l 50.73(a)(2)(ii)(B) 0l 50.73(a)(2)(viii)(B) 0_ 20.2203(a)(2)(i)
El 50.36(c)(1)(i)(A) 0l 50.73(a)(2)(iii)
[1 50.73(a)(2)(ix)(A)
- 10. POWER LEVEL 0l 20.2203(a)(2)(ii)
El 50.36(c)(1)(ii)(A)
Z 50.73(a)(2)(iv)(A)
El 50.73(a)(2)(x) 0l 20.2203(a)(2)(iii) 0l 50.36(c)(2) 0l 50.73(a)(2)(v)(A)
El 73.71 (a)(4) 0l 20.2203(a)(2)(iv)
El 50.46(a)(3)(ii) 0l 50.73(a)(2)(v)(B) 0l 73.71 (a)(5) 100 0l 20.2203(a)(2)(v) 0l 50.73(a)(2)(i)(A) 0l 50.73(a)(2)(v)(C)
El OTHER 0_ 20.2203(a)(2)(vi)
El 50.73(a)(2)(i)(B) 0l 50.73(a)(2)(v)(D) specify inAbstract 3
eo.r i NRC
_________________Fern, 3eeA
- 12. LICENSEE CONTACT FOR THIS LER NAME TELEPHONE NUMBER (Include Area Code)
Steve Austin, Licensing Engineer 256-729-2070CAUSE SYSTEM COMPONENT MANU-REPORTABLE MANU-REPORTABLE FACTURER TO EPIX
CAUSE
SY FACTURER TO EPIX
- 14. SUPPLEMENTAL REPORT EXPECTED
- 15. EXPECTED MONTH DAY YEAR SUBMISSION
[]
YES (If yes, complete 15. EXPECTED SUBMISSION DATE)
ED NO DATE N/A N/A N/A ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines)
On February 16, 2009, at 0513:47 hours Central Standard Time (CST), the Unit 2 reactor was manually scrammed and the turbine tripped in response to excessive stator cooling water temperature and initiation of the automatic turbine trip timer. At 0506 hours0.00586 days <br />0.141 hours <br />8.366402e-4 weeks <br />1.92533e-4 months <br /> CST, operations received a stator cooling water abnormal alarm.
Operations dispatched an auxiliary unit operator to the stator cooling water skid to investigate the alarm. At approximately 0512 hours0.00593 days <br />0.142 hours <br />8.465608e-4 weeks <br />1.94816e-4 months <br /> CST, the idle stator cooling water pump was started. At 0513 hours0.00594 days <br />0.143 hours <br />8.482143e-4 weeks <br />1.951965e-4 months <br />, operations received alarms indicating the stator cooling water outlet temperature had exceeded the high temperature setpoint of 174 degrees F and the automatic turbine trip timer started. As required by Alarm Response Procedure, ARP-9-8A, Operations manually scrammed the reactor and tripped the turbine at 0513:47 hours CST. The root cause of this event was inadequate design of the stator cooling water system. In this event, the temperature controller and TCV-35-54 is a single point failure that led to the manual scram. The stator cooling water temperature control valve, TCV-35-54, is a proportioning valve that directs water flow through the stator cooling water heat exchangers. When the TCV is in the open position, flow bypasses the stator cooling water heat exchangers. In contrast, when the TCV is in the closed position, water flows through the stator cooling water heat exchangers. When the temperature controller failed, TCV-35-54 repositioned to the open position bypassing the heat exchangers. To prevent recurrence of this event, TVA's plans include design and install a temperature controlled solenoid that will vent the actuator air supply to TCV-35-54. Also, install a hand wheel to allow manual control of TCV-35-54.
NRC FORM 366 (6-2004)
I. PLANT CONDITION(S)
Prior to the event, Units 1, 2, and 3 were in operating in Mode 1 at 100 percent thermal power (approximately 3458 megawatts thermal). Units 1 and 3 were unaffected by the event.
II. DESCRIPTION OF EVENT
A. Event-On February 16, 2009, at 0513:47 hours Central Standard Time (CST), the Unit 2 reactor was manually scrammed and the turbine tripped in response to excessive stator cooling water temperature [TJ], and initiation of the automatic turbine trip timer.
At 0506 hours0.00586 days <br />0.141 hours <br />8.366402e-4 weeks <br />1.92533e-4 months <br /> CST, operations received a stator cooling water abnormal alarm. Operations dispatched an auxiliary unit operator to the stator cooling water skid to investigate the alarm.
At approximately 0512 hours0.00593 days <br />0.142 hours <br />8.465608e-4 weeks <br />1.94816e-4 months <br /> CST, the idle stator cooling water pump was started. At 0513 hours0.00594 days <br />0.143 hours <br />8.482143e-4 weeks <br />1.951965e-4 months <br />, operations received alarms indicating the stator cooling water outlet temperature had exceeded the high temperature setpoint of 174 degrees F and the automatic turbine trip timer started. As required by Alarm Response Procedure, ARP-9-8A, Operations manually scrammed the reactor and tripped the turbine at 0513:47 hours CST.
During the event, all automatic functions resulting from the scram occurred as expected. The main turbine generator [TA] tripped. All control rods [AA] inserted. The primary containment isolation system (PCIS) [JE] isolations: Group 2 (residual heat removal (RHR) system [BO]
shutdown cooling), Group 3 (reactor water cleanup (RWCU)) [CE], System Group 6 (ventilation), and Group 8 (traversing incore probe (TIP)) [IG] were received along with the auto start of the control room emergency ventilation (CREV) [VI] system and the three standby gas treatment (SGT) [BH] system trains. As a result of the low reactor water level and high reactor pressure, Operations briefly entered Emergency Operating Instruction, (2-EOI-001)
Reactor Pressure Vessel Control.
The 2-AOl-1 00-1, Reactor Scram, actions were completed as required. Operations reset the reactor scram by 0522 hours0.00604 days <br />0.145 hours <br />8.630952e-4 weeks <br />1.98621e-4 months <br /> CST. By approximately 0540 hours0.00625 days <br />0.15 hours <br />8.928571e-4 weeks <br />2.0547e-4 months <br /> CST, operations reset the PCIS actuations and secured the SGT and CREV systems.
TVA is submitting this report in accordance with 10 CFR 50.73(a)(2)(iv)(A). An event that resulted in a manual or automatic actuation of the systems listed in paragraph 10 CFR 50.73(a)(2)(iv)(B) (i.e., reactor protection system including reactor scram or trip, and general containment isolation signals affecting containment isolation valves in more than one system).
B. Inoperable Structures, Components, or Systems that Contributed to the Event:
None.
C. Dates and ADDroximate Times of Maior Occurrences:
February 16, 2009 0513:47 hours CST Unit 2 reactor manually scrammed.
February 16, 2009 0845 hours0.00978 days <br />0.235 hours <br />0.0014 weeks <br />3.215225e-4 months <br /> CST TVA made a four hour non-emergency report per 10 CFR 50.72(b)(2)(iv)(B) and an eight hour non-emergency report per 10 CFR 50.72(b)(3)(iv)(A).
D. Other Systems or Secondary Functions Affected
None.
E. Method of Discovery
The operations crew received main control room alarms indicating the stator cooling water temperature was abnormal. They also received control room alarm indicating the automatic turbine trip timer had started.
F. Ooerator Actions Operations personnel responded to the event according to applicable plant procedures. They initiated the manual scram as required by the alarm response procedure, Turbine Trip Timer Initiated, ARP-9-8A. Following the manual scram, operations entered AOl-100-1, Reactor Scram.
G. Safety System Responses The RPS logic responded to the reactor scram. All control rods inserted. The PCIS isolations Group 2 (RHR system shutdown cooling), Group 3 (RWCU system), Group 6 (ventilation),
and Group 8 (TIP) isolation were received as expected, due to the lowering of the reactor water level, along with the auto start of the CREV system and the three SGT system trains.
Emergency core cooling system actuation was not required.
Ill. CAUSE OF THE EVENT A. Immediate Cause The immediate cause for the event was the failure of the controller for temperature control valve TCV-35-54. The initial investigation found the controller unresponsive.
B. Root Cause The root cause of this event was inadequate design of the stator cooling water system. The system contains single failure points that can potentially result in a generator trip and subsequent reactor scram. In this event, the temperature controller and TCV-35-54 is the single point failure that required the manual scram.
C. Contributina Factors Failure to recognize that the installation of a mechanical stop on the stator cooling water temperature control valve for protection against actuator spring failure on the temperature control valve was not an adequate solution for plant conditions that existed at the time of the scram.
IV. ANALYSIS OF THE EVENT
The stator cooling water temperature control valve, TCV-35-54, is a proportioning valve that regulates water flow through the stator cooling water heat exchangers. When the TCV is in the open position, flow bypasses the stator cooling water heat exchangers. In contrast, when the TCV is in the closed position, all of the cooling water flows through the heat exchangers. When the temperature controller failed, TCV-35-54 repositioned to the open position bypassing the heat exchangers.
In April of 2001, TVA installed a mechanical stop on the temperature control valve to limit the valve travel in the open position. The stop was set 1/8 inch above the midpoint of the valve travel. In March of 2003, the stop was adjusted to 3/8 inch above the midpoint of the valve travel. This adjustment increased the minimum stator cooling water temperature which at the time, was approximately 10 degrees too low. The investigation into the event determined that the correct mechanical stop position is dependent on many factors, the temperature of the raw cooling water [NG] being the most significant. Regular adjustment of the stop position would be necessary to provide protection against TCV and controller failure. TCV-35-54 was against the mechanical stop following the scram.
V. ASSESSMENT OF SAFETY CONSEQUENCES
The safety consequences of this event were not significant. The manual scram was not complicated. BFN analysis includes a manual scram of the reactor from 100 percent power.
During and following the manual scram, all safety systems operated as required. The operator actions taken in response to the failure of the stator cooling water system and the scram were appropriate. These actions included the verification that the reactor had shutdown, the expected system isolations and indications had occurred, and subsequent restoration of these systems to normal pre-scram alignment.
PCIS groups 2, 3, 6, and 8 isolations were as expected. Although the Emergency Core Cooling Systems were available, none were required. No main steam relief valves [SB] actuated. The turbine bypass valves [JI] maintained reactor pressure. The main condenser remained available for heat rejection. Reactor water level was recovered and maintained by the reactor feed water [SJ] and condensate [SG] systems. Therefore, TVA concludes that the event did not affect the health and safety of the public.
VI. CORRECTIVE ACTIONS
A.
Immediate Corrective Actions
TVA disassembled and inspected TCV-35-54 and did not identify any valve damage. A functional check of the temperature controller was performed. Prior to restart of Unit 2, TCV-35-54 was calibrated. A new position for the mechanical stop on TCV-35-54, 1/4 inch above the midpoint position, was established.
BFN revised the alarm response procedure for a failed temperature control valve or failed temperature controller. Added steps to isolate the air supply to the temperature control valve. This will direct maximum stator cooling water flow to the system heat exchangers.
The revision also included moving the step to commence reduction of generator output to immediately following verification of a valid temperature alarm.
B.
Corrective Actions to Prevent Recurrence 1 To prevent recurrence of this event, TVA plans to design and install a temperature controlled solenoid that will vent the air supply to the actuator on TCV-35-54. TVA also plans to design and install a hand wheel to allow manual control of TCV-35-54.
VII.
ADDITIONAL INFORMATION
A.
Failed Components None.
B.
Previous LERs on Similar Events None.
C.
Additional Information
Corrective action document PER 163680.
D.
Safety System Functional Failure Consideration:
This event is not a safety system functional failure in accordance with NEI 99-02.
E.
Loss of Normal Heat Removal Consideration:
This event was not a complicated scram according to NEI 99-02.
VIII.
COMMITMENTS
None.
TVA does not consider these corrective actions as regulatory requirements. TVA will track the completion of these actions in the Corrective Action Program.
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| 05000259/LER-2009-001, Turbine Trip and Reactor Scram Due to Power Load Unbalance Signal on Main Generator | Turbine Trip and Reactor Scram Due to Power Load Unbalance Signal on Main Generator | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000260/LER-2009-001, Regarding Manual Reactor Scram Following Stator Cooling Water Equipment Failure | Regarding Manual Reactor Scram Following Stator Cooling Water Equipment Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000296/LER-2009-001, Regarding Reactor Scram Due to Loss of Condensate Booster Pumps | Regarding Reactor Scram Due to Loss of Condensate Booster Pumps | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000260/LER-2009-002, Regarding Leak in an ASME Class I Code Reactor Pressure Boundary Pipe | Regarding Leak in an ASME Class I Code Reactor Pressure Boundary Pipe | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - 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Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000259/LER-2009-002, Regarding Unexpected Logic Lockout of the Loop II Residual Heat Removal System Pumps | Regarding Unexpected Logic Lockout of the Loop II Residual Heat Removal System Pumps | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000296/LER-2009-003, Brown Ferry, Unit 3 Re Reactor Core Isolation Cooling System Inoperable Longer than Allowed by the Technical Specifications | Brown Ferry, Unit 3 Re Reactor Core Isolation Cooling System Inoperable Longer than Allowed by the Technical Specifications | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000260/LER-2009-003, Main Steam Relief Valve as Found Setpoint Exceeded Technical Specification Lift Pressure | Main Steam Relief Valve as Found Setpoint Exceeded Technical Specification Lift Pressure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | | 05000259/LER-2009-003, Regarding a Train Standby Gas Treatment System Inoperable Longer than Allowed by the Technical Specifications | Regarding a Train Standby Gas Treatment System Inoperable Longer than Allowed by the Technical Specifications | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000260/LER-2009-004, Regarding Technical Specification Shutdown Due to Rise in Unidentified Drywell Leakage | Regarding Technical Specification Shutdown Due to Rise in Unidentified Drywell Leakage | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000259/LER-2009-004, High Pressure Core Injection Found Inoperable During Compensate Header Level Switch Calibration and Functional Test | High Pressure Core Injection Found Inoperable During Compensate Header Level Switch Calibration and Functional Test | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000259/LER-2009-005-02, Brown Ferry, Unit 1, Regarding Reactor Vessel Water Level 1 Initiation Logic Including the Common Accident Logic Not Evaluated for Appendix R Fire Event | Brown Ferry, Unit 1, Regarding Reactor Vessel Water Level 1 Initiation Logic Including the Common Accident Logic Not Evaluated for Appendix R Fire Event | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000259/LER-2009-005-01, Regarding Reactor Vessel Water Level 1 Initiation Logic Including the Common Accident Logic Not Evaluated for Appendix R Fire Event | Regarding Reactor Vessel Water Level 1 Initiation Logic Including the Common Accident Logic Not Evaluated for Appendix R Fire Event | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000260/LER-2009-005, Reactor Motor Operated Valve Board 2D & Residual Heat Removal Subsystem Inoperable Longer than Allowed by the Plants Technical Specifications | Reactor Motor Operated Valve Board 2D & Residual Heat Removal Subsystem Inoperable Longer than Allowed by the Plants Technical Specifications | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000259/LER-2009-006, Regarding Inoperable High Pressure Coolant Injection Pump Due to Emergency Core Cooling System Inverter Failure | Regarding Inoperable High Pressure Coolant Injection Pump Due to Emergency Core Cooling System Inverter Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000260/LER-2009-006, Automatic Reactor Protection System Scram While Shutdown | Automatic Reactor Protection System Scram While Shutdown | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000259/LER-2009-006-01, 1 for Brown Ferry, Unit 1 Regarding Inoperable High Pressure Coolant Injection Pump Due to Emergency Core Cooling System Inverter Failure | 1 for Brown Ferry, Unit 1 Regarding Inoperable High Pressure Coolant Injection Pump Due to Emergency Core Cooling System Inverter Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000260/LER-2009-007, Regarding Manual Scram During Removal of a Reactor Feedwater Pump from Service | Regarding Manual Scram During Removal of a Reactor Feedwater Pump from Service | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000260/LER-2009-008, Reactor Core Isolation Cooling System Inoperable Longer than Allowed by the Plants Technical Specifications | Reactor Core Isolation Cooling System Inoperable Longer than Allowed by the Plants Technical Specifications | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000260/LER-2009-009, Inadvertent Isolation of the High Pressure Coolant Injection System During Testing Activities | Inadvertent Isolation of the High Pressure Coolant Injection System During Testing Activities | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) |
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