05000296/LER-2008-002, Main Steam Relief Valve as Found Setpoint Exceeded Technical Specification Lift Pressure
| ML082140199 | |
| Person / Time | |
|---|---|
| Site: | Browns Ferry |
| Issue date: | 07/31/2008 |
| From: | West R Tennessee Valley Authority |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| LER 08-002-00 | |
| Download: ML082140199 (8) | |
| Event date: | |
|---|---|
| Report date: | |
| Reporting criterion: | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(ix)(A) 10 CFR 50.73(a)(2)(x) |
| 2962008002R00 - NRC Website | |
text
July 31, 2008 U.S. Nuclear Regulatory Commission 10 CFR 50.73 ATTN: Document Control Desk Mail Stop: OWFN, P1-35 Washington, D. C. 20555-0001
Dear Sir:
TENNESSEE VALLEY AUTHORITY - BROWNS FERRY NUCLEAR PLANT (BFN) -
UNIT 3 - DOCKET 50-296 - FACILITY OPERATING LICENSE DPR LICENSEE EVENT REPORT (LER) 50-296/2008-002 The enclosed report provides details of a failure to meet the requirements of the Technical Specifications (TS) Limiting Condition for Operation (LCO) 3.4.3 concerning the main steam relief valve operability.
TVA is reporting this in accordance with 10 CFR 50.73(a)(2)(i)(B) as an operation or condition prohibited by the plant's TS. There are no commitments contained in this letter.
Sincerely, original signed by S. M. Douglas for R. G. West Site Vice President, BFN cc: See page 2
U.S. Nuclear Regulatory Commission Page 2 July 31, 2008 Enclosure cc (Enclosure):
Ms. Eva Brown, Project Manager U.S. Nuclear Regulatory Commission (MS 08G9)
One White Flint, North 11555 Rockville Pike Rockville, Maryland 20852-2739 Eugene F. Guthrie, Branch Chief U.S. Nuclear Regulatory Commission Region II Sam Nunn Atlanta Federal Center 61 Forsyth Street, SW, Suite 23T85 Atlanta, Georgia 30303-8931 NRC Resident Inspector Browns Ferry Nuclear Plant 10833 Shaw Road Athens, Alabama 35611-6970 (VERIFY)
U.S. Nuclear Regulatory Commission Page 3 July 31, 2008 DTL:JEE:SWA:BDL Enclosure cc (Enclosure):
G. P. Arent, EQB 1B-WBN W. R. Campbell, Jr. LP 3R-C S. M. Douglas, POB 2C-BFN R. F. Marks, Jr., PAB 1C-BFN D. C. Matherly, BFT 2A-BFN L. E. Nicholson, LP 4K-C R. G. West, NAB 2A-BFN B. A. Wetzel, LP 4K-C S. A. Vance, WT 6A-K E. J. Vigluicci, ET 11A-K INPO: LEREvents@inpo.org NSRB Support, LP 5M-C EDMS WT CA-K, S:\\Licensing\\Lic\\Submit\\LERs\\296-2008-002 relief valves.doc
NRC FORM 366 (9-2007)
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (9-2007)
LICENSEE EVENT REPORT (LER)
(See reverse for required number of digits/characters for each block)
APPROVED BY OMB NO. 3150-0104 EXPIRES 08/31/2010
, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
- 1. FACILITY NAME Browns Ferry Unit 3
- 2. DOCKET NUMBER 05000296
- 3. PAGE 1 of 4
- 4. TITLE: Main Steam Relief Valve As Found Setpoint Exceeded Technical Specification Lift Pressure
- 5. EVENT DATE
- 6. LER NUMBER
- 7. REPORT DATE
- 8. OTHER FACILITIES INVOLVED MONTH DAY YEAR YEAR SEQUENTIAL NUMBER REV NO.
MONTH DAY YEAR FACILITY NAME None DOCKET NUMBER N/A 06 02 2008 2008 - 002 - 00 07 31 2008 FACILITY NAME None DOCKET NUMBER N/A
- 9. OPERATING MODE
- 11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply) 1
- 10. POWER LEVEL 100 20.2201(b) 20.2201(d) 20.2203(a)(1) 20.2203(a)(2)(i) 20.2203(a)(2)(ii) 20.2203(a)(2)(iii) 20.2203(a)(2)(iv) 20.2203(a)(2)(v) 20.2203(a)(2)(vi) 20.2203(a)(3)(i) 20.2203(a)(3)(ii) 20.2203(a)(4) 50.36(c)(1)(i)(A) 50.36(c)(1)(ii)(A) 50.36(c)(2) 50.46(a)(3)(ii) 50.73(a)(2)(i)(A) 50.73(a)(2)(i)(B) 50.73(a)(2)(i)(C) 50.73(a)(2)(ii)(A) 50.73(a)(2)(ii)(B) 50.73(a)(2)(iii) 50.73(a)(2)(iv)(A) 50.73(a)(2)(v)(A) 50.73(a)(2)(v)(B) 50.73(a)(2)(v)(C) 50.73(a)(2)(v)(D) 50.73(a)(2)(vii) 50.73(a)(2)(viii)(A) 50.73(a)(2)(viii)(B) 50.73(a)(2)(ix)(A) 50.73(a)(2)(x) 73.71(a)(4) 73.71(a)(5)
OTHER Specify in Abstract below or in (If more space is required, use additional copies of (If more space is required, use additional copies of (If more space is required, use additional copies of NRC Form 366A) (17)
(2) TVA does not consider the corrective action a regulatory requirement. The completion of the action will be tracked in TVA's Corrective Action Program.
VII. ADDITIONAL INFORMATION
A.
Failed Components None.
B.
Previous LERs on Similar Events Numerous previous reports on similar events have been made by BFN. Starting with Unit 1 in the fall of 2008, BFN will implement corrective actions that have been successful at other Boiling Water Reactors. This should help correct the issue at BFN.
C.
Additional Information
Corrective action document for this report is PER 146189.
D.
Safety System Functional Failure Consideration:
This event is not a safety system functional failure according to NEI 99-02.
E.
Scram With Complications Consideration:
This event was not a complicated scram according to NEI 99-02.
VIII. COMMITMENTS
None.