ML16314C026: Difference between revisions

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| number = ML16314C026
| number = ML16314C026
| issue date = 11/08/2016
| issue date = 11/08/2016
| title = Comanche Peak Nuclear Power Plant - NRC Integrated Inspection Report 05000445/2016003 and 05000446/2016003
| title = NRC Integrated Inspection Report 05000445/2016003 and 05000446/2016003
| author name = Groom J R
| author name = Groom J
| author affiliation = NRC/RGN-IV/DRP/RPB-A
| author affiliation = NRC/RGN-IV/DRP/RPB-A
| addressee name = Peters K
| addressee name = Peters K
Line 14: Line 14:
| page count = 29
| page count = 29
}}
}}
See also: [[followed by::IR 05000445/2016003]]
See also: [[see also::IR 05000445/2016003]]


=Text=
=Text=
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION IV 1600 E. LAMAR BLVD. ARLINGTON, TX 76011-4511 November 8, 2016 Mr. Ken Peters, Senior Vice President  and Chief Nuclear Officer TEX Operations Company LLC P.O. Box 1002 Glen Rose, TX 76043 SUBJECT: COMANCHE PEAK NUCLEAR POWER PLANT - NRC INTEGRATED INSPECTION REPORT 05000445/2016003 and 05000446/2016003 Dear Mr. Peters: On September 30, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Comanche Peak Nuclear Power Plant, Units 1 and 2. On September 29, 2016, the NRC inspectors discussed the results of this inspection with Mr. S. Sewell, Senior Director of Engineering and Regulatory Affairs, and other members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report. NRC inspectors documented two findings of very low safety significance (Green) in this report. All of these findings involved violations of NRC requirements. If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC resident inspector at the Comanche Peak Nuclear Power Plant, Units 1 and 2. If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV; and the NRC resident inspector at the Comanche Peak Nuclear Power Plant, Units 1 and 2. In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, "Public Inspections, Exemptions, Requests for Withholding," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC's Public Document Room or from the Publicly Available Records (PARS) component of the NRC's  
{{#Wiki_filter:UNITED STATES
K. Peters - 2 - Agencywide Documents Access and Management System (ADAMS).  ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). Sincerely, /RA/ Jeremy R. Groom, Branch Chief Project Branch A Division of Reactor Projects Docket Nos.  50-445 and 50-446  License Nos. NPF-87 and NPF-89 Enclosure: Inspection Report 05000445/2016003 and    05000446/2016003 w/ Attachment:  Supplemental Information cc w/ encl:  Electronic Distribution 
                            NUCLEAR REGULATORY COMMISSION
                                                REGION IV
                                          1600 E. LAMAR BLVD.
                                        ARLINGTON, TX 76011-4511
                                          November 8, 2016
Mr. Ken Peters, Senior Vice President
   and Chief Nuclear Officer
TEX Operations Company LLC
P.O. Box 1002
Glen Rose, TX 76043
SUBJECT:       COMANCHE PEAK NUCLEAR POWER PLANT - NRC INTEGRATED
                INSPECTION REPORT 05000445/2016003 and 05000446/2016003
Dear Mr. Peters:
On September 30, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an
inspection at your Comanche Peak Nuclear Power Plant, Units 1 and 2. On September 29,
2016, the NRC inspectors discussed the results of this inspection with Mr. S. Sewell, Senior
Director of Engineering and Regulatory Affairs, and other members of your staff. Inspectors
documented the results of this inspection in the enclosed inspection report.
NRC inspectors documented two findings of very low safety significance (Green) in this report.
All of these findings involved violations of NRC requirements.
If you contest the violations or significance of these NCVs, you should provide a response within
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with
copies to the Regional Administrator, Region IV; the Director, Office of Enforcement,
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC resident
inspector at the Comanche Peak Nuclear Power Plant, Units 1 and 2.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a
response within 30 days of the date of this inspection report, with the basis for your
disagreement, to the Regional Administrator, Region IV; and the NRC resident inspector at the
Comanche Peak Nuclear Power Plant, Units 1 and 2.
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public
Inspections, Exemptions, Requests for Withholding, a copy of this letter, its enclosure, and your
response (if any) will be available electronically for public inspection in the NRCs Public
Document Room or from the Publicly Available Records (PARS) component of the NRC's


  SUNSI Review By:  JRG ADAMS  Yes    No  Non-Sensitive  Sensitive  Publicly Available  Non-Publicly Available Keyword: NRC-002 OFFICE SRI:DRP/A RI:DRP/A SPE:DRP/A BC:EB1 BC:EB2 BC:OB BC:PSB2 NAME JJosey RKumana RAlexander TFarnholtz GWerner VGaddy HGepford SIGNATURE /RA/ /RA/ /RA/ /RA/ /RA/ /RA/ /
K. Peters                                    -2-
Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible
from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic
Reading Room).
                                          Sincerely,
                                          /RA/
                                          Jeremy R. Groom, Branch Chief
                                          Project Branch A
                                          Division of Reactor Projects
Docket Nos. 50-445 and 50-446
License Nos. NPF-87 and NPF-89
Enclosure:
Inspection Report 05000445/2016003 and
  05000446/2016003
w/ Attachment: Supplemental Information
cc w/ encl: Electronic Distribution
 
 
 
  SUNSI Review        ADAMS          Non-Sensitive  Publicly Available          Keyword:
  By: JRG                Yes  No      Sensitive        Non-Publicly Available    NRC-002
  OFFICE      SRI:DRP/A    RI:DRP/A  SPE:DRP/A    BC:EB1    BC:EB2        BC:OB      BC:PSB2
  NAME        JJosey      RKumana    RAlexander    TFarnholtz GWerner        VGaddy      HGepford
  SIGNATURE /RA/            /RA/      /RA/          /RA/      /RA/          /RA/        /RA/
  DATE        10/21/16    10/24/16  10/19/16      10/19/16  10/25/16      10/20/16    10/20/16
  OFFICE      TL-IPAT      BC:DRP/A
  NAME        THipschman JGroom
  SIGNATURE /RA/            /RA/
  DATE        10/19/16    11/8/16
                                     
Letter to Ken Peters from Jeremy Groom dated November 8, 2016
SUBJECT: COMANCHE PEAK NUCLEAR POWER PLANT-NRC INTEGRATED
            INSPECTION REPORT 05000445/2016003 and 05000446/2016003
DISTRIBUTION:
Regional Administrator (Kriss.Kennedy@nrc.gov)
Deputy Regional Administrator (Scott.Morris@nrc.gov)
DRP Director (Troy.Pruett@nrc.gov)
DRP Deputy Director (Ryan.Lantz@nrc.gov)
DRS Director (Anton.Vegel@nrc.gov)
DRS Deputy Director (Jeff.Clark@nrc.gov)
Senior Resident Inspector (Jeffrey.Josey@nrc.gov)
Resident Inspector (Rayomand.Kumana@nrc.gov)
Administrative Assistant (VACANT)
Branch Chief, DRP/A (Jeremy.Groom@nrc.gov)
Senior Project Engineer, DRP/A (Ryan.Alexander@nrc.gov)
Project Engineer, DRP/A (Thomas.Sullivan@nrc.gov)
Project Engineer, DRP/A (Mathew.Kirk@nrc.gov)
Public Affairs Officer (Victor.Dricks@nrc.gov)
Project Manager (Margaret.Watford@nrc.gov)
Team Leader, DRS/IPAT (Thomas.Hipschman@nrc.gov)
RITS Coordinator (Marisa.Herrera@nrc.gov)
ACES (R4Enforcement.Resource@nrc.gov)
Regional Counsel (Karla.Fuller@nrc.gov)
Congressional Affairs Officer (Jenny.Weil@nrc.gov)
RIV Congressional Affairs Officer (Angel.Moreno@nrc.gov)
RIV/ETA: OEDO (Jeremy.Bowen@nrc.gov)
ROPreports
Electronic Distribution for Comanche Peak Nuclear Power Plant
 
            U.S. NUCLEAR REGULATORY COMMISSION
                              REGION IV
Docket:    05000445, 05000446
License:    NPF-87, NPF-89
Report:    05000445/2016003 and 05000446/2016003
Licensee:  TEX Operations Company, LLC
Facility:  Comanche Peak Nuclear Power Plant, Units 1 and 2
Location:  6322 N. FM-56, Glen Rose, Texas
Dates:      July 1 through September 30, 2016
Inspectors: J. Josey, Senior Resident Inspector
            R. Kumana, Resident Inspector
            W. Cullum, Reactor Inspector
Approved    Jeremy R. Groom
    By:    Chief, Project Branch A
            Division of Reactor Projects
                                  A-1                        Attachment
 
                                              SUMMARY
IR 05000445/2016003 and 05000446/2016003; 07/01/2016 - 09/30/2016; Comanche Peak
NPP, Units 1 and 2; Maintenance Effectiveness, Problem Identification and Resolution
The inspection activities described in this report were performed between July 1, 2016, through
September 30, 2016, by the resident inspectors at the Comanche Peak Nuclear Power Plant
and an inspector from the NRCs Region IV office. Two findings of very low safety significance
(Green) are documented in
}}
}}

Latest revision as of 12:13, 30 October 2019

NRC Integrated Inspection Report 05000445/2016003 and 05000446/2016003
ML16314C026
Person / Time
Site: Comanche Peak  Luminant icon.png
Issue date: 11/08/2016
From: Jeremy Groom
NRC/RGN-IV/DRP/RPB-A
To: Peters K
TEX Operations Company
JEREMY GROOM
References
IR 2016003
Download: ML16314C026 (29)


See also: IR 05000445/2016003

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION IV

1600 E. LAMAR BLVD.

ARLINGTON, TX 76011-4511

November 8, 2016

Mr. Ken Peters, Senior Vice President

and Chief Nuclear Officer

TEX Operations Company LLC

P.O. Box 1002

Glen Rose, TX 76043

SUBJECT: COMANCHE PEAK NUCLEAR POWER PLANT - NRC INTEGRATED

INSPECTION REPORT 05000445/2016003 and 05000446/2016003

Dear Mr. Peters:

On September 30, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Comanche Peak Nuclear Power Plant, Units 1 and 2. On September 29,

2016, the NRC inspectors discussed the results of this inspection with Mr. S. Sewell, Senior

Director of Engineering and Regulatory Affairs, and other members of your staff. Inspectors

documented the results of this inspection in the enclosed inspection report.

NRC inspectors documented two findings of very low safety significance (Green) in this report.

All of these findings involved violations of NRC requirements.

If you contest the violations or significance of these NCVs, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with

copies to the Regional Administrator, Region IV; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC resident

inspector at the Comanche Peak Nuclear Power Plant, Units 1 and 2.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region IV; and the NRC resident inspector at the

Comanche Peak Nuclear Power Plant, Units 1 and 2.

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public

Inspections, Exemptions, Requests for Withholding, a copy of this letter, its enclosure, and your

response (if any) will be available electronically for public inspection in the NRCs Public

Document Room or from the Publicly Available Records (PARS) component of the NRC's

K. Peters -2-

Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible

from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic

Reading Room).

Sincerely,

/RA/

Jeremy R. Groom, Branch Chief

Project Branch A

Division of Reactor Projects

Docket Nos. 50-445 and 50-446

License Nos. NPF-87 and NPF-89

Enclosure:

Inspection Report 05000445/2016003 and

05000446/2016003

w/ Attachment: Supplemental Information

cc w/ encl: Electronic Distribution

SUNSI Review ADAMS Non-Sensitive Publicly Available Keyword:

By: JRG Yes No Sensitive Non-Publicly Available NRC-002

OFFICE SRI:DRP/A RI:DRP/A SPE:DRP/A BC:EB1 BC:EB2 BC:OB BC:PSB2

NAME JJosey RKumana RAlexander TFarnholtz GWerner VGaddy HGepford

SIGNATURE /RA/ /RA/ /RA/ /RA/ /RA/ /RA/ /RA/

DATE 10/21/16 10/24/16 10/19/16 10/19/16 10/25/16 10/20/16 10/20/16

OFFICE TL-IPAT BC:DRP/A

NAME THipschman JGroom

SIGNATURE /RA/ /RA/

DATE 10/19/16 11/8/16

Letter to Ken Peters from Jeremy Groom dated November 8, 2016

SUBJECT: COMANCHE PEAK NUCLEAR POWER PLANT-NRC INTEGRATED

INSPECTION REPORT 05000445/2016003 and 05000446/2016003

DISTRIBUTION:

Regional Administrator (Kriss.Kennedy@nrc.gov)

Deputy Regional Administrator (Scott.Morris@nrc.gov)

DRP Director (Troy.Pruett@nrc.gov)

DRP Deputy Director (Ryan.Lantz@nrc.gov)

DRS Director (Anton.Vegel@nrc.gov)

DRS Deputy Director (Jeff.Clark@nrc.gov)

Senior Resident Inspector (Jeffrey.Josey@nrc.gov)

Resident Inspector (Rayomand.Kumana@nrc.gov)

Administrative Assistant (VACANT)

Branch Chief, DRP/A (Jeremy.Groom@nrc.gov)

Senior Project Engineer, DRP/A (Ryan.Alexander@nrc.gov)

Project Engineer, DRP/A (Thomas.Sullivan@nrc.gov)

Project Engineer, DRP/A (Mathew.Kirk@nrc.gov)

Public Affairs Officer (Victor.Dricks@nrc.gov)

Project Manager (Margaret.Watford@nrc.gov)

Team Leader, DRS/IPAT (Thomas.Hipschman@nrc.gov)

RITS Coordinator (Marisa.Herrera@nrc.gov)

ACES (R4Enforcement.Resource@nrc.gov)

Regional Counsel (Karla.Fuller@nrc.gov)

Congressional Affairs Officer (Jenny.Weil@nrc.gov)

RIV Congressional Affairs Officer (Angel.Moreno@nrc.gov)

RIV/ETA: OEDO (Jeremy.Bowen@nrc.gov)

ROPreports

Electronic Distribution for Comanche Peak Nuclear Power Plant

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 05000445, 05000446

License: NPF-87, NPF-89

Report: 05000445/2016003 and 05000446/2016003

Licensee: TEX Operations Company, LLC

Facility: Comanche Peak Nuclear Power Plant, Units 1 and 2

Location: 6322 N. FM-56, Glen Rose, Texas

Dates: July 1 through September 30, 2016

Inspectors: J. Josey, Senior Resident Inspector

R. Kumana, Resident Inspector

W. Cullum, Reactor Inspector

Approved Jeremy R. Groom

By: Chief, Project Branch A

Division of Reactor Projects

A-1 Attachment

SUMMARY

IR 05000445/2016003 and 05000446/2016003; 07/01/2016 - 09/30/2016; Comanche Peak

NPP, Units 1 and 2; Maintenance Effectiveness, Problem Identification and Resolution

The inspection activities described in this report were performed between July 1, 2016, through

September 30, 2016, by the resident inspectors at the Comanche Peak Nuclear Power Plant

and an inspector from the NRCs Region IV office. Two findings of very low safety significance

(Green) are documented in this report. Both of these findings involved a violation of NRC

requirements. The significance of inspection findings is indicated by their color (Green, White,

Yellow, or Red), which is determined using Inspection Manual Chapter 0609, Significance

Determination Process. Their cross-cutting aspects are determined using Inspection Manual

Chapter 0310, Aspects within the Cross-Cutting Areas. Violations of NRC requirements are

dispositioned in accordance with the NRC Enforcement Policy. The NRCs program for

overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process.

Cornerstone: Initiating Events

  • Green. The inspectors identified a non-cited violation of 10 CFR 50.65(a)(4), Requirements

for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, for the licensees

failure to adequately manage the increase in risk associated with the potential for a loss of

decay heat removal during refueling outages. Specifically, the licensee implemented a risk

management action that did not reduce the risk, but instead called for placing a safety

injection pump in service during periods where this action is prohibited by plants technical

specifications for low temperature over pressure protection. The inspectors determined this

was an ineffective risk management action because the use of a safety injection pump

during low pressure and temperature conditions would place the plant in an unanalyzed

condition, resulting in an increase in risk. As an immediate corrective action, the licensee

initiated Condition Report CR-2015-009109 to evaluate appropriate risk management

actions. This finding was entered into the licensees corrective action program as Condition

Report CR-2015-009109.

The failure to manage the increase in risk associated with the potential for a loss of decay

heat removal during refueling activities is a performance deficiency. The performance

deficiency was more than minor, and therefore a finding, because it was associated with the

procedure quality attribute of the Initiating Events Cornerstone and affected the cornerstone

objective to limit the likelihood of events that upset plant stability and challenge critical safety

functions during shutdown as well as power operations. Using Inspection Manual Chapter 0609, Appendix K, Maintenance Risk Assessment and Risk Management Significance

Determination Process, dated May 19, 2005, Flowchart 1, Assessment of Risk Deficit, the

inspectors determined the need to calculate the risk deficit to determine the significance of

this issue. A senior reactor analyst performed a bounding qualitative assessment and

determined the incremental core damage probability deficit was less than 1E-6 and the

incremental large early release probability deficit was less than 1E-7, based on the

availability of additional equipment to mitigate the loss of decay heat removal. In

accordance with Flowchart 1 in Appendix K, because incremental core damage probability

deficit was less than 1E-6 and incremental large early release probability deficit was less

than 1E-7, the finding screened as having very low safety significance (Green). The finding

has a human performance cross-cutting aspect associated with bases for decisions, in that,

the licensee failed to ensure that operations leadership adequately communicate potential

A-2

problems with the risk management action to start a safety injection pump when in a mode

of applicability for low temperature over pressure protection [H.10]. (Section 4OA2)

Cornerstone: Mitigating Systems

  • Green. The inspectors identified a non-cited violation of 10 CFR 50.65(a)(2), Requirements

for monitoring the effectiveness of maintenance at nuclear power plants. Specifically, the

licensee failed to demonstrate that the performance of the Unit 2 auxiliary feedwater check

valves was being effectively controlled through the performance of appropriate preventive

maintenance. The licensees failure to perform appropriate maintenance resulted in several

failures of the check valves. The licensee entered this issue into corrective action program

as CR-2016-008312.

The licensees failure to effectively monitor the performance of maintenance rule scoped

equipment in accordance with 10 CFR 50.65(a)(2) was a performance deficiency. The

performance deficiency was more than minor, and therefore a finding, because it was

associated with the equipment performance attribute of the Mitigating Systems Cornerstone

and affected the cornerstone objective to ensure availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences. Specifically,

the licensee failed to demonstrate that the performance of the Unit 2 auxiliary feedwater

check valves was being effectively controlled through the performance of appropriate

preventive maintenance which resulted in failures of the valves. Using Inspection Manual

Chapter (IMC) 0609, Appendix A, The Significance Determination Process (SDP) for

Findings At-Power, dated June 19, 2012, inspectors determined that this finding was of

very low safety significance (Green) because the finding (1) was not a deficiency affecting

the design and qualification of a mitigating structure, system, or component, and did not

result in a loss of operability or functionality, (2) did not represent a loss of system and/or

function, (3) did not represent an actual loss of function of at least a single train for longer

than its allowed outage time, or two separate safety systems out-of-service for longer than

their technical specification allowed outage time, and (4) did not represent an actual loss of

function of one or more non-technical specification trains of equipment designated as high

safety-significant for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in accordance with the licensees maintenance

rule program. A cross-cutting aspect was not assigned to this finding because the

performance deficiency occurred in 1996, and therefore, is not indicative of current licensee

performance. (Section 1R12)

Licensee-Identified Violations

None

A-3

PLANT STATUS

Unit 1 and Unit 2 began the inspection period at approximately 100 percent power and operated

at that power level for the entire inspection period.

REPORT DETAILS

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

.1 Summer Readiness for Offsite and Alternate AC Power Systems

a. Inspection Scope

On July 20, 2016, the inspectors completed an inspection of the stations off-site and

alternate-ac power systems. The inspectors inspected the material condition of these

systems, including transformers and other switchyard equipment to verify that plant

features and procedures were appropriate for operation and continued availability of off-

site and alternate-ac power systems. The inspectors reviewed outstanding work orders

and open condition reports for these systems. The inspectors walked down the

switchyard to observe the material condition of equipment providing off-site power

sources. The inspectors verified that the licensees procedures included appropriate

measures to monitor and maintain availability and reliability of the off-site and alternate-

ac power systems.

These activities constituted one sample of summer readiness of off-site and alternate-ac

power systems, as defined in Inspection Procedure 71111.01.

b. Findings

No findings were identified.

1R04 Equipment Alignment (71111.04)

.1 Partial Walk-Down

a. Inspection Scope

The inspectors performed partial system walk-downs of the following risk-significant

systems:

pumps

  • August 23, 2016, Unit 1, train A 125 VDC distribution system
  • September 20, 2016, Units 1 and 2, fire protection piping in the service water

intake structure

A-4

The inspectors reviewed the licensees procedures and system design information to

determine the correct lineup for the systems. They visually verified that critical portions

of the systems or trains were correctly aligned for the existing plant configuration.

These activities constituted three partial system walk-down samples as defined in

Inspection Procedure 71111.04.

b. Findings

No findings were identified.

1R05 Fire Protection (71111.05)

.1 Quarterly Inspection

a. Inspection Scope

The inspectors evaluated the licensees fire protection program for operational status

and material condition. The inspectors focused their inspection on four plant areas

important to safety:

room

injection, containment spray pumps rooms

  • September 19, 2016, Fire area SE16, Unit 1 Electrical Equipment Room
  • September 19, 2016, Fire area 2SE16, Unit 2 Electrical Equipment Room

For each area, the inspectors evaluated the fire plan against defined hazards and

defense-in-depth features in the licensees fire protection program. The inspectors

evaluated control of transient combustibles and ignition sources, fire detection and

suppression systems, manual firefighting equipment and capability, passive fire

protection features, and compensatory measures for degraded conditions.

These activities constituted four quarterly inspection samples, as defined in Inspection

Procedure 71111.05.

b. Findings

No findings were identified.

A-5

.2 Annual Inspection

a. Inspection Scope

On September 20, 2016, the inspectors completed their annual evaluation of the

licensees fire brigade performance. This evaluation included observation of two fire

drills:

  • March 22, 2016, Unit 1, announced drill, contaminated waste fire drill, 832 foot

corridor

  • June 22, 2016, Unit 2, announced drill, 858 foot elevation valve gallery

During these drills the inspectors evaluated the capability of the fire brigade members,

the leadership ability of the brigade leader, the brigades use of turnout gear and fire-

fighting equipment, and the effectiveness of the fire brigades team operation. The

inspectors also reviewed whether the licensees fire brigade met NRC requirements for

training, dedicated size and membership, and equipment.

These activities constituted one annual inspection sample, as defined in Inspection

Procedure 71111.05.

b. Findings

No findings were identified.

1R06 Flood Protection Measures (71111.06)

a. Inspection Scope

On September 23, 2016, the inspectors completed an inspection of the stations ability to

mitigate flooding due to internal causes. After reviewing the licensees flooding analysis,

the inspectors selected one plant area containing risk-significant structures, systems,

and components that were susceptible to flooding:

The inspectors reviewed plant design features and licensee procedures for coping with

internal flooding. The inspectors walked down the selected areas to inspect the design

features, including the material condition of seals, drains, and flood barriers. The

inspectors evaluated whether operator actions credited for flood mitigation could be

successfully accomplished.

These activities constituted completion of one flood protection measures sample as

defined in Inspection Procedure 71111.06.

b. Findings

No findings were identified.

A-6

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

(71111.11)

.1 Review of Licensed Operator Requalification

a. Inspection Scope

On September 27, 2016, the inspectors observed a portion of an annual requalification

test for licensed operators. The inspectors assessed the performance of the operators

and the evaluators critique of their performance.

These activities constituted completion of one quarterly licensed operator requalification

program sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

.2 Review of Licensed Operator Performance

a. Inspection Scope

Inspectors observed the performance of on-shift licensed operators in the plants main

control room. At the time of the observations, the plant was in a period of heightened

activity or risk due to testing being performed on reactor protection and response to

unusual plant conditions. The inspectors observed the operators performance of the

following activities:

  • July 13, 2016, Unit 2, Observation during slave relay testing
  • August 8, 2016, Unit 2, Observation of operators response to heater drain pump

seal water low pressure alarm

  • September 26, 2016, Unit 1, Observation of reactor trip breaker testing

In addition, the inspectors assessed the operators adherence to plant procedures,

including conduct of operations procedure and other operations department policies.

These activities constituted completion of one quarterly licensed operator performance

sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors reviewed two instances of degraded performance or condition of safety-

related structures, systems, and components (SSCs):

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  • September 23, 2016, Unit 1, pressurizer heater group C blown fuse

The inspectors reviewed the extent of condition of possible common cause SSC failures

and evaluated the adequacy of the licensees corrective actions. The inspectors

reviewed the licensees work practices to evaluate whether these may have played a

role in the degradation of the SSCs. The inspectors assessed the licensees

characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance

Rule), and verified that the licensee was appropriately tracking degraded performance

and conditions in accordance with the Maintenance Rule.

These activities constituted completion of two maintenance effectiveness samples, as

defined in Inspection Procedure 71111.12.

b. Findings

Introduction. The inspectors identified a Green, non-cited violation of 10 CFR

50.65(a)(2), Requirements for monitoring the effectiveness of maintenance at nuclear

power plants. Specifically, the licensee failed to demonstrate that the performance of

the Unit 2 auxiliary feedwater check valves was being effectively controlled through the

performance of appropriate preventive maintenance.

Description. On November 11, 2015, the licensee conducted in-service testing on

feedwater check valve 2FW-0191, one of four steam generator split flow bypass check

valves. During the test, check valve 2FW-0191 failed to meet the sites acceptance

criteria indicating the valve failed to seat. The licensee stopped the test and initiated

Condition Report CR-2015-10961 to document the test failure.

Subsequently, the system engineer performed a maintenance rule functional failure

review of this issue. This review determined that the failure of valve 2FW-0191 to seat

was not a maintenance rule functional failure and the function would remain in (a)(2)

status. Inspectors questioned this assessment because one of the scoped functions of

this feedwater check valve is to shut to prevent bypassing flow from the steam

generators. During discussions with the licensee, the inspectors determined that system

engineer was only evaluating the split flow check valves performance against the main

feedwater systems criteria to provide feedwater to the steam generator, and not against

the criteria related to the valves ability to shut to prevent bypassing flow from the steam

generators. Inspectors also determined that the licensee was not performing

preventative maintenance on the check valves to ensure their ability to close and seat

properly.

The inspectors subsequently reviewed the last test data for all four of the steam

generator split flow bypass check valves. In this review the inspectors noted that in

2011 valve 2FW-0192 had failed to meet the established acceptance criteria, yet the

failure was not noted as a functional failure. Additionally, in 2012, valves 2FW-0191,

2FW-0192, and 2FW-0193 all failed to meet the established acceptance criteria, and

again the failures were not noted as functional failures.

The inspectors noted that 10 CFR 50.65(a)(2) requires, in part, that monitoring as

specified in 10 CFR 50.65(a)(1) is not required where it has been demonstrated that the

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performance of a system is being effectively controlled through the performance of

appropriate preventive maintenance, such that the system remains capable of

performing its intended function. Based on their review, the inspectors determined that

the licensee failed to demonstrate that the performance of the Unit 2 feedwater check

valves was being effectively controlled. Specifically, the licensee was not performing

preventative maintenance on the check valves, resulting in the valves failing to close on

multiple occasions during testing.

The inspectors informed the licensee of the concerns and the licensee initiated condition

report CR-2016-008312 to capture this issue in the stations corrective action program.

The licensee recognized that they were not correctly monitoring the function of these

check valves. Specifically, the licensee determined that monitoring the check valves

only as part of the main feedwater system was not adequate since the systems

performance criteria is to provide feedwater to the steam generators, and the check

valves function is to close to prevent bypass flow. The licensee subsequently performed

a review to determine if other safety-related check valves were also not being monitored

correctly. Based on this review the licensee determined that there were 841 safety-

related check valves (of which 230 were classified as run to failure) that were not being

monitored against their scoped criteria. To correct this issue, the licensee created a new

monitoring function for safety related check valves which monitors the close function,

and moved the equipment to 10 CFR 50.65(a)(1) monitoring requirements because they

determined that they were not able to demonstrate that the performance of the check

valves was being effectively controlled.

Analysis. The licensees failure to effectively monitor the performance of maintenance

rule scoped equipment in accordance with 10 CFR 50.65(a)(2) was a performance

deficiency. The performance deficiency was more than minor, and therefore a finding,

because it was associated with the equipment performance attribute of the Mitigating

Systems Cornerstone and affected the cornerstone objective to ensure availability,

reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. Specifically, the licensee failed to demonstrate that the

performance of the Unit 2 auxiliary feedwater check valves was being effectively

controlled through the performance of appropriate preventive maintenance which

resulted in failures of the valves. Using Inspection Manual Chapter (IMC) 0609,

Appendix A, The Significance Determination Process (SDP) for Findings At-Power,

dated June 19, 2012, inspectors determined that this finding was of very low safety

significance (Green) because the finding (1) was not a deficiency affecting the design

and qualification of a mitigating structure, system, or component, and did not result in a

loss of operability or functionality, (2) did not represent a loss of system and/or function,

(3) did not represent an actual loss of function of at least a single train for longer than its

allowed outage time, or two separate safety systems out-of-service for longer than their

technical specification allowed outage time, and (4) did not represent an actual loss of

function of one or more non-technical specification trains of equipment designated as

high safety-significant for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in accordance with the licensees

maintenance rule program. A cross-cutting aspect was not assigned to this finding

because the performance deficiency occurred in 1996 when the steam generator split

flow bypass check valve was initially scoped under the Maintenance Rule, and therefore,

is not indicative of current licensee performance.

Enforcement. Title 10 CFR 50.65(a)(1) requires, in part, that holders of an operating

license shall monitor the performance of systems and components against licensee

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established goals, in a manner sufficient to provide reasonable assurance that such

structures, systems, and components are capable of fulfilling their intended safety

functions. 10 CFR 50.65(a)(2) states, in part, that monitoring as specified in 10 CFR

50.65(a)(1) is not required where it has been demonstrated that the performance of a

system is being effectively controlled through the performance of appropriate preventive

maintenance, such that the system remains capable of performing its intended function.

Contrary to the above, from initial maintenance rule scoping in 1996 to September 2016,

the licensee did not monitor the performance of the Unit 2 auxiliary feedwater system

check valves against licensee-established goals in a manner sufficient to provide

reasonable assurance that the check valves were capable of fulfilling their intended

safety functions, and the licensee did not demonstrate that the performance of check

valves was being effectively controlled through the performance of appropriate

preventive maintenance, such that the system remained capable of performing its

intended function. In response to this issue the licensee created a new monitoring

function for safety related check valves, and moved the equipment to 10 CFR

50.65(a)(1) monitoring requirements pending further review. Since this violation was of

very low safety significance (Green) and has been entered into the corrective action

program as Condition Report CR-2016-008312, this violation is being treated as a non-

cited violation consistent with Section 2.3.2 of the NRC Enforcement Policy.

(NCV 05000446/2016003-01, Failure to Adequately Monitor Feedwater System Check

Valve Performance)

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

On July 7, 2016, the inspectors reviewed a risk assessment and the risk management

actions taken by the licensee in response to elevated risk associated with performing an

oil sample on spent fuel pool pump X-01.

The inspectors verified that this risk assessment was performed timely and in

accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant

procedures. The inspectors reviewed the accuracy and completeness of the licensees

risk assessment and verified that the licensee implemented appropriate risk

management actions based on the result of the assessment.

The inspectors also observed portions of three emergent work activities that had the

potential to affect the functional capability of mitigating systems:

  • August 18, 2016, Unit 2, Steam generator blowdown isolation valve 2-HV-2399

elastomer replacement

turbine driven auxiliary feedwater pumps

  • September 16, 2016, Unit 2, loop A safety chiller emergent maintenance

The inspectors verified that the licensee appropriately developed and followed a work

plan for these activities. The inspectors verified that the licensee took precautions to

minimize the impact of the work activities on unaffected SSCs.

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These activities constituted completion of four maintenance risk assessments and

emergent work control inspection samples, as defined in Inspection Procedure 71111.13.

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments (71111.15)

a. Inspection Scope

The inspectors reviewed seven operability determinations that the licensee performed

for degraded or nonconforming SSCs:

conditioner X-01 partial refrigerant charge

2-01 86-2 lockout relay actuation

auxiliary feedwater pump 1-01 indicating light socket/bulb melted

auxiliary feedwater pump room heat up analyses

pump 2-01 oil leak

generator 2-01 failed KVAR meter

feedwater pumps following identification of an unanalyzed condition

The inspectors reviewed the timeliness and technical adequacy of the licensees

evaluations. Where the licensee determined the degraded SSC to be operable the

inspectors verified that the licensees compensatory measures were appropriate to

provide reasonable assurance of operability. The inspectors verified that the licensee

had considered the effect of other degraded conditions on the operability of the

degraded SSC.

These activities constituted completion of seven operability and functionality review

samples, as defined in Inspection Procedure 71111.15.

b. Findings

No findings were identified.

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1R18 Plant Modifications (71111.18)

.1 Temporary Modifications

a. Inspection Scope

On September 15, 2016, the inspectors reviewed a temporary plant modification to

remove sentinel valves from the turbine driven auxiliary feedwater pumps on Unit 1

and 2.

The inspectors verified that the licensee had installed these temporary modifications in

accordance with technically adequate design documents. The inspectors verified that

these modifications did not adversely impact the operability or availability of affected

SSCs. The inspectors reviewed design documentation and plant procedures affected by

the modifications to verify the licensee maintained configuration control.

These activities constituted completion of one sample of temporary modifications, as

defined in Inspection Procedure 71111.18.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed four post-maintenance testing activities that affected risk-

significant SSCs:

2-HV-2399 testing following elastomer replacement

following temporary modification

The inspectors reviewed licensing and design-basis documents for the SSCs and the

maintenance and post-maintenance test procedures. The inspectors observed the

performance of the post-maintenance tests to verify that the licensee performed the tests

in accordance with approved procedures, satisfied the established acceptance criteria,

and restored the operability of the affected SSCs.

These activities constituted completion of four post-maintenance testing inspection

samples, as defined in Inspection Procedure 71111.19.

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b. Findings

No findings were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors observed four risk-significant surveillance tests and reviewed test results

to verify that these tests adequately demonstrated that the SSCs were capable of

performing their safety functions:

Other surveillance tests:

  • May 26, 2016, Unit 1, stroke test of power operated relief valve 1-PCV-456
  • August 5, 2016, Unit 2, start and flow test of the turbine driven auxiliary

feedwater pump

  • August 23, 2016, Unit 1, stroke test of containment sump pump discharge line

outside-containment isolation valve 1-HV-5157

  • September 8, 2016, Unit 2, start test of diesel generator 2-01

The inspectors verified that these tests met technical specification requirements, that the

licensee performed the tests in accordance with their procedures, and that the results of

the test satisfied appropriate acceptance criteria. The inspectors verified that the

licensee restored the operability of the affected SSCs following testing.

These activities constituted completion of four surveillance testing inspection samples,

as defined in Inspection Procedure 71111.22.

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation (71114.06)

.1 Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors observed an emergency preparedness drill on September 28, 2016, to

verify the adequacy and capability of the licensees assessment of drill performance.

The inspectors reviewed the drill scenario, observed the drill from the simulator and

emergency operations facility, and attended the post-drill critique. The inspectors

verified that the licensees emergency classifications, off-site notifications, and protective

action recommendations were appropriate and timely. The inspectors verified that any

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emergency preparedness weaknesses were appropriately identified by the licensee in

the post-drill critique and entered into the corrective action program for resolution.

These activities constituted completion of one emergency preparedness drill observation

sample, as defined in Inspection Procedure 71114.06.

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Security

4OA1 Performance Indicator Verification (71151)

.1 Mitigating Systems Performance Index: Emergency AC Power Systems (MS06)

a. Inspection Scope

The inspectors reviewed the licensees mitigating system performance index data for the

period of July 1, 2015 through June 30, 2016 to verify the accuracy and completeness of

the reported data. The inspectors used definitions and guidance contained in Nuclear

Energy Institute Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constituted verification of the mitigating system performance index for

emergency ac power systems for Units 1 and 2, as defined in Inspection

Procedure 71151.

b. Findings

No findings were identified.

.2 Mitigating Systems Performance Index: High Pressure Injection Systems (MS07)

a. Inspection Scope

The inspectors reviewed the licensees mitigating system performance index data for the

period of July 1, 2015 through June 30, 2016 to verify the accuracy and completeness of

the reported data. The inspectors used definitions and guidance contained in Nuclear

Energy Institute Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constituted verification of the mitigating system performance index for

high pressure injection systems for Units 1 and 2, as defined in Inspection

Procedure 71151.

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b. Findings

No findings were identified.

.3 Mitigating Systems Performance Index: Heat Removal Systems (MS08)

a. Inspection Scope

The inspectors reviewed the licensees mitigating system performance index data for the

period of July 1, 2015 through June 30, 2016 to verify the accuracy and completeness of

the reported data. The inspectors used definitions and guidance contained in Nuclear

Energy Institute Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constituted verification of the mitigating system performance index for

heat removal systems for Units 1 and 2, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution (71152)

.1 Routine Review

a. Inspection Scope

Throughout the inspection period, the inspectors performed daily reviews of items

entered into the licensees corrective action program and periodically attended the

licensees condition report screening meetings. The inspectors verified that licensee

personnel were identifying problems at an appropriate threshold and entering these

problems into the corrective action program for resolution. The inspectors verified that

the licensee developed and implemented corrective actions commensurate with the

significance of the problems identified. The inspectors also reviewed the licensees

problem identification and resolution activities during the performance of the other

inspection activities documented in this report.

b. Findings

No findings were identified.

.2 Annual Follow-up of Selected Issues

a. Inspection Scope

The inspectors selected two issues for an in-depth follow-up:

  • During refueling outage 2RF15, October 2015, and refueling outage 1RF18,

May 2016, the licensee credited defense in depth contingency plans, risk

assessments with specified risk management actions, for time periods when the

reactor coolant system would be in a loops not filled condition or when shutdown

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cooling would be in a reduced availability condition due to the increase in risk for

the activities.

The inspectors assessed the licensees risk assessments and the specified risk

management actions. The inspectors identified that the licensee failed to

appropriately manage the risk associated with the activities.

  • On May 18, 2016, after completion of preventative maintenance on the lube oil

cooler for coolant charging pump 1-01, a service water leak was discovered

coming from the cooler head. Upon disassembly, the licensee discovered

significant pitting on the head for the heat exchanger. The licensee initiated

Condition Report 2016-004868 to evaluate the issue, though an operability

evaluation was not performed at the time because the unit was not in a mode of

applicability for the charging pump. The licensee determined that this condition

had been previously identified in Condition Report CR-2014-001804, and parts

were on order to replace the pitted head. The licensees corrective action was to

apply Loctite #2, a sealant material, to stop the leak, noting that this had

previously been evaluated as acceptable in Condition Report CR-2006-001208.

Upon further review inspectors determined that the evaluation performed in CR-

2006-001208 was a one-time evaluation for use of Loctite #2, and did not

establish a basis for the current use. Therefore, an operability evaluation was

required for the subsequent use of Loctite. The licensee initiated Condition

Reports CR-2016-004936 and CR-2016-006674 to address this issue, and

documented a current operability evaluation for use of the Loctite.

Inspectors determined that this issue was a minor violation of Title 10 CFR Part

50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, which

requires, in part, that activities affecting quality shall be accomplished in

accordance with documented instructions, procedures, or drawings, of a type

appropriate to the circumstances. Station Procedure STI-442.01, Operability

Determination and Functionality Assessment Program, is an Appendix B quality

related procedure that is appropriate to the circumstances for evaluating the

operability of safety-related components. Station Procedure STI-442.01 step 6.1,

requires, in part, that when a potential degraded or nonconforming condition is

identified, the shift manager should ensure the operability determination process

is initiated to determine the operability of the structure, system or component.

The inspectors assessed the licensees problem identification threshold, cause

analyses, extent of condition reviews and compensatory actions. The inspectors

verified that the licensee appropriately prioritized the planned corrective actions

and that these actions were adequate to correct the condition.

These activities constituted completion of two annual follow-up sample as defined in

Inspection Procedure 71152.

b. Findings

Introduction. The inspectors identified a Green non-cited violation of

10 CFR 50.65(a)(4), Requirements for Monitoring the Effectiveness of Maintenance at

Nuclear Power Plants, for the licensees failure to adequately manage the increase in

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risk associated with the potential for a loss of decay heat removal during refueling

outages.

Description. During refueling outage 2RF15, October 2015, when the licensee was

setting up for vacuum fill of the reactor coolant system, inspectors reviewed the stations

defense in depth contingency plan 2RF15-01. The inspectors determined that this

contingency plan was a risk assessment with specified risk management actions for

periods when the reactor coolant system would be in a loops not filled condition or

periods of reduced availability of the shutdown cooling system. Inspectors noted that the

contingency plan for these periods of increased risk directed that if residual heat removal

(shutdown cooling) is lost, operators should establish alternate cooling flow path using

Station Procedure ABN-104, Residual Heat Removal System Malfunction, Revision 9,

section 8.

Inspectors reviewed ABN-104, section 8 and noted that it directed operators to start a

safety injection pump in response to a loss of shutdown cooling. Inspectors identified a

concern that the action to start a safety injection pump would occur while in the mode of

applicability for technical specification 3.4.12, Low Temperature Overpressure

Protection System. Technical specification 3.4.12 requires the safety injection pumps

be made incapable of injecting due to concerns of over pressurizing the reactor coolant

system in modes 4, 5, and 6 (the latter only when the reactor vessel head is installed).

The licensee initiated Condition Report CR-2015-009109 to capture the inspectors

concern in the stations corrective action program.

Subsequently, during refueling outage 1RF18, May 2016, inspectors noted that the

licensee again credited a defense in depth contingency plan (1RF18-01) which again

would have operators start a safety injection pump when technical specification 3.4.12

was in effect. During subsequent reviews, the inspectors determined that the licensee

did not have an evaluation for starting a safety injection pump when low temperature

overpressure protection was in effect.

Inspectors determined that the specified risk management action to start a safety

injection pump would restore flow to the core to mitigate the loss of shutdown cooling.

However, the inspectors also determined that the plant is not analyzed for using a safety

injection pump during periods when the reactor coolant system is at low temperatures

requiring low temperature overpressure protection. The proposed use of safety injection

pumps as described in ABN-104, section 8, without analyses for sufficient relief

capability, created the potential for vessel overpressurization and a challenge to the

reactor coolant system barrier. Any challenge to the reactor coolant system barrier

would serve to increase risk. The inspectors also noted that the licensee had several

options to mitigate a potential loss of shutdown cooling that are analyzed during period

where low temperature overpressure protection is required. Specifically, the inspectors

identified that the licensee could start centrifugal charging pumps to restore core flow

following a loss of shutdown cooling. These pumps have slightly less capacity than the

safety inspection pumps which would be bounded by the relief capability required in

technical specification 3.4.12.

Inspectors informed the licensee of the additional concerns and the licensee added them

to Condition Report CR-2015-009109. Inspectors determined that the licensee had not

started a safety injection pump when technical specification 3.4.12 was in effect during

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1RF19 or 2RF18. As corrective actions, the licensee amended Condition Report

CR-2015-009109 to evaluate appropriate risk management actions.

Analyses. The failure to manage the increase in risk associated with the potential for a

loss of decay heat removal during refueling activities is a performance deficiency. The

performance deficiency was more than minor, and therefore a finding, because it was

associated with the procedure quality attribute of the Initiating Events Cornerstone and

affected the cornerstone objective to limit the likelihood of events that upset plant

stability and challenge critical safety functions during shutdown as well as power

operations. Using Inspection Manual Chapter 0609, Appendix K, Maintenance Risk

Assessment and Risk Management Significance Determination Process, dated May 19,

2005, Flowchart 1, Assessment of Risk Deficit, and determined the need to calculate

the risk deficit to determine the significance of this issue. A senior reactor analyst

performed a bounding qualitative assessment, using insights from Inspection Manual

Chapter 0609, Appendix G, Shutdown Operations Significance Determination Process,

and determined the incremental core damage probability deficit was less than 1E-6 and

the incremental large early release probability deficit was less than 1E-7. The influential

assumptions used by the senior reactor analyst included the low exposure time that the

plant is in LTOP conditions, the initiating event frequency associated with a loss of decay

heat removal, available operator mitigation actions that would prevent the use of safety

injection pumps, and the availability of additional equipment to mitigate the loss of decay

heat removal.

In accordance with Flowchart 1 in Appendix K, because incremental core damage

probability deficit was less than 1E-6 and incremental large early release probability

deficit was less than 1E-7, the finding screened as having very low safety significance

(Green). The finding has a human performance cross-cutting aspect associated with

bases for decisions, in that, the licensee failed to ensure that operations leadership

adequately communicate potential problems with the risk management action to start a

safety injection pump when in a mode of applicability for low temperature over pressure

protection [H.10].

Enforcement. Title 10 CFR 50.65(a)(4) requires, in part, that licensees shall assess and

manage the increase in risk that may result from proposed maintenance activities.

Defense in depth contingency plans 2RF15-01 and 1RF18-01 implement pre-planned

risk assessments and specified risk management actions for times during refueling

outages when the reactor coolant system is depressurized and level is lowered.

Contrary to the above, from October 3, 2015, through May 31, 2016, the licensee failed

to manage the increase in risk from proposed maintenance activities. Specifically, the

licensee implemented a risk management action that did not reduce the risk, instead it

called for placing the plant in an unanalyzed condition which could elevate risk. As an

immediate corrective action the licensee initiated Condition Report CR-2015-009109 to

evaluate appropriate risk management actions. Since this violation was of very low

safety significance (Green) and has been entered into the corrective action program as

Condition Report CR-2015-009109, this violation is being treated as a non-cited violation

consistent with Section 2.3.2 of the NRC Enforcement Policy.

(NCV 05000445/2016003-02; 05000446/2016003-02, Failure to Manage Risk During

Refueling Outages)

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4OA5 Other Activities

a. Inspection Scope

The inspectors evaluated the impact of financial conditions on continued safe

performance at Comanche Peak. In that the licensees parent company, Energy Future

Holdings, was under bankruptcy protection/reorganization during the inspection period,

NRC Region IV conducted special reviews of processes at Comanche Peak. The

inspectors evaluated several aspects of the licensees operations to determine whether

the financial condition of the station impacted plant safety. The factors reviewed

included: (1) impact on staffing, (2) corrective maintenance backlog, (3) changes to the

planned maintenance schedule, (4) corrective action program implementation, and

(5) reduction in outage scope, including risk-significant modifications. In particular, the

inspectors verified that licensee personnel continued to identify problems at an

appropriate threshold and enter these problems into the corrective action program for

resolution. The inspectors also verified that the licensee continued to develop and

implement corrective actions commensurate with the significance of the problems

identified.

The special review of processes at Comanche Peak included continuous reviews by the

Resident Inspectors, as well as the specialist-led baseline inspections completed during

the inspection period which are documented previously in this report.

b. Findings

No findings were identified.

4OA6 Meetings, Including Exit

Exit Meeting Summary

On July 7, 2016, the resident inspectors presented the inspection results to Mr. S. Sewell,

Senior Director of Engineering and Regulatory Affairs, and other members of the licensee staff.

The licensee acknowledged the issues presented. The licensee confirmed that any proprietary

information reviewed by the inspectors had been returned or destroyed.

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SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

G. Struble, Manager, Operations/Simulator Training

J. Alldredge, Technician, Radiation Protection

T. Curtis, Lead Environmental Technician

S. Darter, Coordinator, Radiation Protection

S. Dixon, Consulting Licensing Analyst/Regulatory Affairs

T. Emery, Technician, Radiological Environmental Monitoring Program

T. Hope, Manager, Regulatory Affairs

B. Knapp, Acting Manager, Radiation Protection

M. Macho, Supervisor, Radiation Protection

S. Peterson, Senior Calibration Laboratory Technician, Radiation Protection

K. Powell, Supervisor, Radiation Protection

M. Syed, Engineer, Systems Engineer

M. Watkins, Lead Technician, Instruments and Controls Maintenance

J. Barnette, Consultant, Licensing Technologist

S. Bartholomew, Analyst, Emergency Preparedness

G. Bryan, Operations Specialist, Emergency Preparedness

K. Faver, Planner, Emergency Preparedness

R. Fishencord, Planner, Emergency Preparedness

J. Hull, Manager, Emergency Preparedness

R. Marquez, Planner, Emergency Preparedness

S. Sewell, Senior Director of Engineering and Regulatory Affairs

D. Volkening, Manager, Nuclear Oversight

T. McCool, Site Vice President

B. Knowles, Radiation Protection Staff

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

Failure to Adequately Monitor Feedwater System Check Valve

05000446/2016003-01 NCV

Performance (Section 1R12)

05000445/2016003-

Failure to Manage Risk During Refueling Outages (Section

02;05000446/2016003- NCV

4OA2)

02

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LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

Procedures

Number Title Revision

STA-629 Switchyard Control and Transmission Grid Interface 7

Section 1R04: Equipment Alignment

Condition Reports

CR-2016-007245

Drawings

Number Title Revision

E1-0020 125V DC One Line Diagram CP-20

E1-0021 Common Auxiliary Control Fuel and Turbine Buildings Normal CP-22

480VC MCCs One Line Diagram

Procedures

Number Title Revision

SOP-904 Fire Protection Main Water Supply and Fire Pumps System 16

OPT-215 Class 1E Electrical Systems Operability 15

Section 1R05: Fire Protection

Condition Reports

CR-2016-002654

Drawings

Number Title Revision

E1-2020 Safeguard Building Fire Detection Plan EL 773-0, 790-6 and CP-2

800-6

Procedures

Number Title Revision

SAF-104 Inspection of Respiratory Protection Equipment (Maintenance 11

and Repair)

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Procedures

Number Title Revision

ABN-901 Fire Protection System Alarms or Malfunctions 2

FPI-103A Fire Preplan Instruction Manual, Unit 1 Safeguards Building 4

Elevation 810-6, Rad. Pen. Area & Elec. Equip. Rm

Miscellaneous Documents

Number Title Revision

-- Fire Protection Report 30

Work Orders

4789803

Section 1R06: Flood Protection Measures

Calculations

Number Title Revision

SI-CA-0000-693 Miscellaneous Building - Flooding Analysis 1

Section 1R11: Licensed Operator Requalification Program and Licensed Operator

Performance

Procedures

Number Title Revision

EOP-3.0A Steam Generator Tube Rupture 9

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Condition Reports

CR-2016-007272 CR-2016-000493 CR-2016-007720 CR-2016-007428 CR-2016-007690

Procedures

Number Title Revision

DID XPWR-SFP- SFP Cooling During Non-Refueling Outage Conditions -

01

STI-600.01 Protecting Plant Equipment and Sensitive Equipment Controls 1

MSM-GO-0213 Sway Strut Maintenance 1

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Work Orders

5320735 5210636

Section 1R15: Operability Determinations and Functionality Assessments

Calculations

Number Title Revision

1-EB-302-4 As Built HVAC Calculation - Auxiliary Feedwater Pump Room 5

Unit 1

Condition Reports

CR-2016-003089 CR-2016-007251 CR-2016-007653 CR-2016-007840

Work Orders

5010266

Section 1R18: Plant Modifications

Miscellaneous Documents

Number Title Revision

FDA-2016- Create Temp Mod FDA to Remove the Sentinel Valves on the 00

000123-01-00 Casing of the TDAFW Pump Turbines

Work Orders

5330786 5330788

Section 1R19: Post-Maintenance Testing

Condition Reports

CR-2016-000493 CR-2016-007559 TR-2016-004759 CR-2016-005744 CR-2016-005216

CR-2016-003163

Drawings

Number Title Revision

E1-0031-07 6.9 kV Switchgear Bus 1EA2 Breaker 1EA2-2 Schematic CP-13

Diagram

A-23

Procedures

Number Title Revision

MSM-G0-0213 Sway Strut Maintenance 1

MSM-G0-4004 Baker On-line Motor Testing 5

MSM-C0-7310 Service Water Pump Maintenance 5

SOP-603A 6900 V Switchgear 16

MSE-G0-0020 Relay Calibration 5

Work Orders

5210636 5330786 4297555 5008028 4947477

4986918 5008083 5136434 4913385

Section 1R22: Surveillance Testing

Condition Reports

CR-2016-007588

Drawings

Number Title Revision

M2-0206 Flow Diagram Auxiliary Feedwater System CP-15

Procedures

Number Title Revision

OPT-206B AFW System 22

OPT-503A Cntmt Isol Valves ASME Testing 15

Work Orders

5270846

Section 1EP6: Drill Evaluation

Procedures

Number Title Revision

EPP-121 Re-Entry, Recovery and Closeout 10

EPP-116 Emergency Repair & Damage Control and Immediate Entries 9

A-24

Procedures

Number Title Revision

EPP-109 Duties and Responsibilities of the Emergency Coordinator / 15

Recovery Manager

ABN-907 Acts of Nature 15

Section 4OA2: Problem Identification and Resolution

Condition Reports

CR-2006-001208 CR-2014-001804 CR-2016-004868 CR-2016-004936

A-25