PNO-IV-86-023, on 860708,facility Experienced Reactor Scram Due to MSIV Closure at 65% Power.Isolation Initiated Due to Turbine Bldg High Temp Resulting from Manway Gasket Failure. Personnel Evacuated: Difference between revisions

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July 9, 1986 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE -- PNO-IV-86-23 This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. The information is as initially received without verification or evaluation, and is basically all that is known by the Region IV staff on this date.
FACILITY: Gulf States Utilities                          Licensee Emergency Classification:
River Bend Station                              Notification of Unusual Event St. Francisville, Louisiana                    Alert DN: 50-458                                      Site Area Emergency General Emergency X Not Applicable
 
==SUBJECT:==
MAJOR STEAM LEAK RESULTING IN PLANT SHUTDOWN On July 8,1986, at 12:25 CDT, the licensee experienced a reactor scram due to a main steamline isolation valve (MSIV) closure while at 65 percent power.
This isolation initiated due to turbine building high temperature resulting from a manway gasket failure on a moisture separator reheater (MSR) drain tank. The plant responded as expected and no emergency core cooling system (ECCS) initiations were experienced. During the initial transient, two safety relief valves (SRV) lifted, limiting reactor peak pressure to 1086 psig. The reactor core isolation cooling (RCIC) system was placed on line to control reactor pressure. Reactor water level was controlled using the reactor feed pump (RFP). As a result of the steam leay the turbine building ventilation, radiation monitor i                                microcuries per mililiter to a maximumof2.49x10-greasedfrom1.58x10-
                                                      . Plant personnel were evacuated from the turbine building and no injuries occurred. The unit is presently shutdown while the licensee investigates the cause of the manway gasket failure. The resident inspectors will be monitoring the licensee's actions.
The RIV Project Inspector, the NRR Project Manager, and a lead BWR instructor from the Training Center are onsite, i
Neither the licensee nor the NRC plans to issue a press release.
I Region IV received notification of this occurrence by telephone from I          ;            Headquarters Duty officer at approximately 1:30 p.m. CDT on July 8,1986 .
Region IV briefed IE, NRR, PA, and the Commissioners Assistants at I
3:30 p.m. CDT.
            $f 6
CONTACT:
DISTRIBUTION:
G. L. Constable (FTS 728-8151) n                                                                        MAIL:
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{gH.St.                              NNBB          E/W          Willste      ADM:DMB (Original) 00T:(Transonly)
;                  e    Chairman Zech            ED0          IE          NMSS ag$ Com. Bernthal                  PA            OIA          RES
              ,f        Com. Roberts              ELD          AE00                        FAX:
.        ~ ~          Com. Asselstine          MPA          VIB                        TWO
        $'            ACRS                                                                NSAC i jff                  SECY                      Phillips                                  RRI                        rh j                      CA                        NRR                                      SP          (Air Rights)    s& lg l
PDR                      DCS LICENSEE:                ( g\
l                                / Regional Offices                                          (ReactorLicensee) i                          RIV:j    P                RA      A F                            (Transmitted via 5520 - 7/9/86 EHJo    on:cs            RDM 7/10/p                    7/10                                                        11:04a - Jc)
 
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Latest revision as of 19:43, 7 December 2021

PNO-IV-86-023:on 860708,facility Experienced Reactor Scram Due to MSIV Closure at 65% Power.Isolation Initiated Due to Turbine Bldg High Temp Resulting from Manway Gasket Failure. Personnel Evacuated
ML20202D753
Person / Time
Site: River Bend Entergy icon.png
Issue date: 07/09/1986
From: Constable G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
References
PNO-IV-86-023, PNO-IV-86-23, NUDOCS 8607140209
Download: ML20202D753 (1)


-

July 9, 1986 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE -- PNO-IV-86-23 This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. The information is as initially received without verification or evaluation, and is basically all that is known by the Region IV staff on this date.

FACILITY: Gulf States Utilities Licensee Emergency Classification:

River Bend Station Notification of Unusual Event St. Francisville, Louisiana Alert DN: 50-458 Site Area Emergency General Emergency X Not Applicable

SUBJECT:

MAJOR STEAM LEAK RESULTING IN PLANT SHUTDOWN On July 8,1986, at 12:25 CDT, the licensee experienced a reactor scram due to a main steamline isolation valve (MSIV) closure while at 65 percent power.

This isolation initiated due to turbine building high temperature resulting from a manway gasket failure on a moisture separator reheater (MSR) drain tank. The plant responded as expected and no emergency core cooling system (ECCS) initiations were experienced. During the initial transient, two safety relief valves (SRV) lifted, limiting reactor peak pressure to 1086 psig. The reactor core isolation cooling (RCIC) system was placed on line to control reactor pressure. Reactor water level was controlled using the reactor feed pump (RFP). As a result of the steam leay the turbine building ventilation, radiation monitor i microcuries per mililiter to a maximumof2.49x10-greasedfrom1.58x10-

. Plant personnel were evacuated from the turbine building and no injuries occurred. The unit is presently shutdown while the licensee investigates the cause of the manway gasket failure. The resident inspectors will be monitoring the licensee's actions.

The RIV Project Inspector, the NRR Project Manager, and a lead BWR instructor from the Training Center are onsite, i

Neither the licensee nor the NRC plans to issue a press release.

I Region IV received notification of this occurrence by telephone from I  ; Headquarters Duty officer at approximately 1:30 p.m. CDT on July 8,1986 .

Region IV briefed IE, NRR, PA, and the Commissioners Assistants at I

3:30 p.m. CDT.

$f 6

CONTACT:

DISTRIBUTION:

G. L. Constable (FTS 728-8151) n MAIL:

l

{gH.St. NNBB E/W Willste ADM:DMB (Original) 00T:(Transonly)

e Chairman Zech ED0 IE NMSS ag$ Com. Bernthal PA OIA RES

,f Com. Roberts ELD AE00 FAX:

. ~ ~ Com. Asselstine MPA VIB TWO

$' ACRS NSAC i jff SECY Phillips RRI rh j CA NRR SP (Air Rights) s& lg l

PDR DCS LICENSEE: ( g\

l / Regional Offices (ReactorLicensee) i RIV:j P RA A F (Transmitted via 5520 - 7/9/86 EHJo on:cs RDM 7/10/p 7/10 11:04a - Jc)

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