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| issue date = 06/09/1982
| issue date = 06/09/1982
| title = Responds to NRC 820510 Ltr Re Violations Noted in IE Insp Rept 50-280/82-58.Corrective Action Is:Prestartup Checklist Will Be Performed by Instrument Supervisor & All Employees Counseled Re Procedural Compliance
| title = Responds to NRC 820510 Ltr Re Violations Noted in IE Insp Rept 50-280/82-58.Corrective Action Is:Prestartup Checklist Will Be Performed by Instrument Supervisor & All Employees Counseled Re Procedural Compliance
| author name = LEASBURG R H
| author name = Leasburg R
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
| addressee name = DEYOUNG R C
| addressee name = Deyoung R
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
| docket = 05000280, 05000281
| docket = 05000280, 05000281
Line 14: Line 14:
| page count = 3
| page count = 3
}}
}}
See also: [[followed by::IR 05000280/1982058]]


=Text=
=Text=
{{#Wiki_filter:** ,,/' * e * VIRGINIA ELECTRIC AND POWER COMPANY RlCHMOND.., VJRGlNlA 23261 R. H. LEASBURO VJCE PRESIDENT  
{{#Wiki_filter:e                                  *
NuCLEAJ< OPERATIONS  
,,/'
June 9, 1982 United States Nuclear Regulatory  
R. H. LEASBURO VIRGINIA ELECTRIC AND POWER COMPANY RlCHMOND.., VJRGlNlA 23261 June 9, 1982        IE HQ Fl'LE *OOP'r VJCE PRESIDENT NuCLEAJ< OPERATIONS United States Nuclear Regulatory Commission                     Serial No. 301 Attn: Mr. Richard C. DeYoung, Director                           NO/RMT:acm Office of Inspection and Enforcement                   Docket No. 50-280 Washington, D.C. 20555                                           License No. DPR-32 Gentlemen:
Commission  
We have reviewed your letter of May 10, 1982 in reference to the inspection conducted at Surry Power* Station on February 23 and 24, 1982 and reported in IE Inspection Report No. EA 82-58. Our response to the specific infraction is attached.
Attn: Mr. Richard C. DeYoung, Director Office of Inspection  
While we accept full responsibility for this incident, we believe further consideration should be given by the NRC to the following two items.
and Enforcement  
(1) This incident was discovered and promptly reported by VEPCO.
Washington, D.C. 20555 Gentlemen:
(2) The NRC agreed with our earlier actions regarding the August, 1980 incident which caused a 25 percent increase in the civil penalty. The preventive measures implemented as a result of that incident were prudent measures and could be reasonably expected to prevent items in the future.
IE HQ Fl'LE *OOP'r Serial No. 301 NO/RMT:acm
The preventive measures were vigorously implemented.
Docket No. 50-280 License No. DPR-32 We have reviewed your letter of May 10, 1982 in reference  
We believe the above two items, properly considered by the NRC should cause remission or mitigation of the penalty. We would be pleased to discuss this further if necessary.
to the inspection  
We have determined that no proprietary information is contained in the report.
conducted  
Accordingly, the Virginia Electric and Power Company has no objection to this inspection report being made a matter of public disclosure. The information contained in the attached pages is true and accurate to the best of my knowledge and belief.
at Surry Power* Station on February 23 and 24, 1982 and reported in IE Inspection  
Enclosures
Report No. EA 82-58. Our response to the specific infraction  
: 1. Response to Notice of Violation
is attached.  
: 2. Voucher Check No. 28825 in payment of Civil Penalty cc: Mr. James P. O'Reilly Regional Administrator, Region II 8206160306 820609 PDR ADOCK 05000280
While we accept full responsibility  
_9~_*. _*__ _         PDR
for this incident, we believe further consideration  
 
should be given by the NRC to the following  
e J     J J.,.
two items. (1) This incident was discovered  
Attachment Serial No. 301 RESPONSE TO NOTICE OF VIOLATION INSPECTION REPORT NOS. 50-280/82-58 NRC COMMENT Technical Specification 6.4.D requires the licensee to follow procedures established in compliance with Technical Specifications 6.4.A. Procedure 5.2 of Section 14 of the Quality Assurance Manual was established to implement 6.4.A. Paragraph 5.2.2 of this procedure requires that jumpers not controlled by an approved procedure shall not be used anywhere in the station without the Shift Supervisor's prior knowledge and approval.
and promptly reported by VEPCO. (2) The NRC agreed with our earlier actions regarding  
Technical Specification 3.7.B requires the licensee to have an operable high steam flow channel in each main steamline when the reactor coolant system temperature is above 543&deg;F.
the August, 1980 incident which caused a 25 percent increase in the civil penalty. The preventive  
Contrary to the above, on February 21, 1982 the licensee did not implement procedure 5.2 of Section 14 of the approved Quality Assurance Manual in that fuses were pulled without the benefit of an approved procedure and without the knowl~dge and approval, of the Shift* Supervisor. Jumpers a1? used in this procedure include, but are not limited to electrical lifted leads. In this instance, the removal of fuses is considered the equivalent of lifting electrical leads. As a consequence, Unit 1 was operated, between 4:00 p.m. on February 21 and 2:45 a.m. on February 22, without an operable high steam flow channel in "A" main steamline when the reactor coolant system temperature was above 543&deg;F .
measures implemented  
* This is a Severity Level III Violation (Supplement I)
as a result of that incident were prudent measures and could be reasonably  
(Civil Penalty - $50,000)
expected to prevent items in the future. The preventive  
 
measures were vigorously  
===RESPONSE===
implemented.  
: 1. ADMISSION OR DENIAL OF THE ALLEGED VIOLATION:
We believe the above two items, properly considered  
The violation is correct as stated. It is important to note that the error in each case was licensee identified before the reactor had reached the power range and the absence of the fuses would have been self-disclosing. Immediate corrective action was taken. Additionally, the incident resulted from failure to follow procedures which had been modified to preclude such an event. In light of the above, Vepco considers these events not to be symptomatic of basic flaws in the Safety Program but rather isolated occurrences admittedly similar in nature.
by the NRC should cause remission  
: 2. REASONS FOR VIOLATION:
or mitigation  
The violation is resultant from an individual's failure to follow procedural controls.
of the penalty. We would be pleased to discuss this further if necessary.  
: 3. CORRECTIVE STEPS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED:
We have determined  
Subsequent to this event additional procedural controls were implemented
that no proprietary  
* to 1) clarify the requirement for using approved jumpers for pulled fuses, and 2) include a pre-start up checklist to be performed by an Instrument Supervisor which verifies proper alignment of all reactor protection and engineered safeguards instrumentation. In addition, emphasis on procedural compliance has been stressed to all station employees. These
information  
__ J
is contained  
 
in the report. Accordingly, the Virginia Electric and Power Company has no objection  
                                                                                          -~1
to this inspection  
~ - .-.   ~
report being made a matter of public disclosure.  
J e                                       Attachment Page 2 I
The information  
Serial No. 301
contained  
* 4.
in the attached pages is true and accurate to the best of my knowledge  
actions have provided an effective program that ensures proper system alignment and operator awareness of procedural requirements and system status.
and belief. Enclosures  
CORRECTIVE STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:
1. Response to Notice of Violation  
Engineering is conducting a review to determine if design changes to this and similar systems will mitigate the opportunity for this type of incident.
2. Voucher Check No. 28825 in payment of Civil Penalty cc: Mr. James P. O'Reilly Regional Administrator, Region II 8206160306  
: 5. DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED:
820609 PDR ADOCK 05000280 _9~_*. _*__ _ PDR
Full complia~ce hap been achieved .
J J ;, J.,. * * * e RESPONSE TO NOTICE OF VIOLATION  
*}}
INSPECTION  
REPORT NOS. 50-280/82-58  
Attachment
Serial No. 301 NRC COMMENT Technical  
Specification  
6.4.D requires the licensee to follow procedures  
established  
in compliance  
with Technical  
Specifications  
6.4.A. Procedure  
5.2 of Section 14 of the Quality Assurance  
Manual was established  
to implement  
6.4.A. Paragraph  
5.2.2 of this procedure  
requires that jumpers not controlled  
by an approved procedure  
shall not be used anywhere in the station without the Shift Supervisor's  
prior knowledge  
and approval.  
Technical  
Specification  
3.7.B requires the licensee to have an operable high steam flow channel in each main steamline  
when the reactor coolant system temperature  
is above 543&deg;F. Contrary to the above, on February 21, 1982 the licensee did not implement  
procedure  
5.2 of Section 14 of the approved Quality Assurance  
Manual in that fuses were pulled without the benefit of an approved procedure  
and without the knowl~dge  
and approval, of the Shift* Supervisor.  
Jumpers a1? used in this procedure  
include, but are not limited to electrical  
lifted leads. In this instance, the removal of fuses is considered  
the equivalent  
of lifting electrical  
leads. As a consequence, Unit 1 was operated, between 4:00 p.m. on February 21 and 2:45 a.m. on February 22, without an operable high steam flow channel in "A" main steamline  
when the reactor coolant system temperature  
was above 543&deg;F . This is a Severity Level III Violation (Supplement  
I) (Civil Penalty -$50,000) RESPONSE:  
1. ADMISSION  
OR DENIAL OF THE ALLEGED VIOLATION:  
The violation  
is correct as stated. It is important  
to note that the error in each case was licensee identified  
before the reactor had reached the power range and the absence of the fuses would have been self-disclosing.  
Immediate  
corrective  
action was taken. Additionally, the incident resulted from failure to follow procedures  
which had been modified to preclude such an event. In light of the above, Vepco considers  
these events not to be symptomatic  
of basic flaws in the Safety Program but rather isolated occurrences  
admittedly  
similar in nature. 2. REASONS FOR VIOLATION:  
3. The violation  
is resultant  
from an individual's  
failure to follow procedural  
controls.  
CORRECTIVE  
STEPS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED:  
Subsequent  
to this event additional  
procedural  
controls were implemented  
to 1) clarify the requirement  
for using approved jumpers for pulled fuses, and 2) include a pre-start  
up checklist  
to be performed  
by an Instrument  
Supervisor  
which verifies proper alignment  
of all reactor protection  
and engineered  
safeguards  
instrumentation.  
In addition, emphasis on procedural  
compliance  
has been stressed to all station employees.  
These __ J   
--. J . * * * * e Attachment  
Page 2 Serial No. 301 actions have provided an effective  
program that ensures proper system alignment  
and operator awareness  
of procedural  
requirements  
and system status. 4. CORRECTIVE  
STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:  
Engineering  
is conducting  
a review to determine  
if design changes to this and similar systems will mitigate the opportunity  
for this type of incident.  
5. DATE WHEN FULL COMPLIANCE  
WILL BE ACHIEVED:  
Full complia~ce  
hap been achieved . -~1 I
}}

Latest revision as of 05:18, 23 February 2020

Responds to NRC 820510 Ltr Re Violations Noted in IE Insp Rept 50-280/82-58.Corrective Action Is:Prestartup Checklist Will Be Performed by Instrument Supervisor & All Employees Counseled Re Procedural Compliance
ML18139B891
Person / Time
Site: Surry  Dominion icon.png
Issue date: 06/09/1982
From: Leasburg R
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To: Deyoung R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
References
301, NUDOCS 8206160306
Download: ML18139B891 (3)


Text

e *

,,/'

R. H. LEASBURO VIRGINIA ELECTRIC AND POWER COMPANY RlCHMOND.., VJRGlNlA 23261 June 9, 1982 IE HQ Fl'LE *OOP'r VJCE PRESIDENT NuCLEAJ< OPERATIONS United States Nuclear Regulatory Commission Serial No. 301 Attn: Mr. Richard C. DeYoung, Director NO/RMT:acm Office of Inspection and Enforcement Docket No. 50-280 Washington, D.C. 20555 License No. DPR-32 Gentlemen:

We have reviewed your letter of May 10, 1982 in reference to the inspection conducted at Surry Power* Station on February 23 and 24, 1982 and reported in IE Inspection Report No. EA 82-58. Our response to the specific infraction is attached.

While we accept full responsibility for this incident, we believe further consideration should be given by the NRC to the following two items.

(1) This incident was discovered and promptly reported by VEPCO.

(2) The NRC agreed with our earlier actions regarding the August, 1980 incident which caused a 25 percent increase in the civil penalty. The preventive measures implemented as a result of that incident were prudent measures and could be reasonably expected to prevent items in the future.

The preventive measures were vigorously implemented.

We believe the above two items, properly considered by the NRC should cause remission or mitigation of the penalty. We would be pleased to discuss this further if necessary.

We have determined that no proprietary information is contained in the report.

Accordingly, the Virginia Electric and Power Company has no objection to this inspection report being made a matter of public disclosure. The information contained in the attached pages is true and accurate to the best of my knowledge and belief.

Enclosures

1. Response to Notice of Violation
2. Voucher Check No. 28825 in payment of Civil Penalty cc: Mr. James P. O'Reilly Regional Administrator, Region II 8206160306 820609 PDR ADOCK 05000280

_9~_*. _*__ _ PDR

e J J J.,.

Attachment Serial No. 301 RESPONSE TO NOTICE OF VIOLATION INSPECTION REPORT NOS. 50-280/82-58 NRC COMMENT Technical Specification 6.4.D requires the licensee to follow procedures established in compliance with Technical Specifications 6.4.A. Procedure 5.2 of Section 14 of the Quality Assurance Manual was established to implement 6.4.A. Paragraph 5.2.2 of this procedure requires that jumpers not controlled by an approved procedure shall not be used anywhere in the station without the Shift Supervisor's prior knowledge and approval.

Technical Specification 3.7.B requires the licensee to have an operable high steam flow channel in each main steamline when the reactor coolant system temperature is above 543°F.

Contrary to the above, on February 21, 1982 the licensee did not implement procedure 5.2 of Section 14 of the approved Quality Assurance Manual in that fuses were pulled without the benefit of an approved procedure and without the knowl~dge and approval, of the Shift* Supervisor. Jumpers a1? used in this procedure include, but are not limited to electrical lifted leads. In this instance, the removal of fuses is considered the equivalent of lifting electrical leads. As a consequence, Unit 1 was operated, between 4:00 p.m. on February 21 and 2:45 a.m. on February 22, without an operable high steam flow channel in "A" main steamline when the reactor coolant system temperature was above 543°F .

(Civil Penalty - $50,000)

RESPONSE

1. ADMISSION OR DENIAL OF THE ALLEGED VIOLATION:

The violation is correct as stated. It is important to note that the error in each case was licensee identified before the reactor had reached the power range and the absence of the fuses would have been self-disclosing. Immediate corrective action was taken. Additionally, the incident resulted from failure to follow procedures which had been modified to preclude such an event. In light of the above, Vepco considers these events not to be symptomatic of basic flaws in the Safety Program but rather isolated occurrences admittedly similar in nature.

2. REASONS FOR VIOLATION:

The violation is resultant from an individual's failure to follow procedural controls.

3. CORRECTIVE STEPS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED:

Subsequent to this event additional procedural controls were implemented

  • to 1) clarify the requirement for using approved jumpers for pulled fuses, and 2) include a pre-start up checklist to be performed by an Instrument Supervisor which verifies proper alignment of all reactor protection and engineered safeguards instrumentation. In addition, emphasis on procedural compliance has been stressed to all station employees. These

__ J

-~1

~ - .-. ~

J e Attachment Page 2 I

Serial No. 301

  • 4.

actions have provided an effective program that ensures proper system alignment and operator awareness of procedural requirements and system status.

CORRECTIVE STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:

Engineering is conducting a review to determine if design changes to this and similar systems will mitigate the opportunity for this type of incident.

5. DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED:

Full complia~ce hap been achieved .