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| issue date = 02/22/2011
| issue date = 02/22/2011
| title = IR 05000346-11-009(DRS), on 01/14/2011, 01/27/2011, Davis-Besse Nuclear Power Station; Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications
| title = IR 05000346-11-009(DRS), on 01/14/2011, 01/27/2011, Davis-Besse Nuclear Power Station; Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications
| author name = Daley R C
| author name = Daley R
| author affiliation = NRC/RGN-III/DRS/EB3
| author affiliation = NRC/RGN-III/DRS/EB3
| addressee name = Allen B
| addressee name = Allen B
Line 18: Line 18:


=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:ary 22, 2011
[[Issue date::February 22, 2011]]


Mr. Barry Allen Site Vice President FirstEnergy Nuclear Operating Company Davis-Besse Nuclear Power Station 5501 North State Route 2, Mail Stop A-DB-3080 Oak Harbor, OH 43449-9760
==SUBJECT:==
DAVIS-BESSE NUCLEAR POWER STATION, EVALUATIONS OF CHANGES, TESTS, OR EXPERIMENTS AND PERMANENT PLANT MODIFICATIONS BASELINE INSPECTION REPORT 05000346/2011009(DRS)


SUBJECT: DAVIS-BESSE NUCLEAR POWER STATION, EVALUATIONS OF CHANGES, TESTS, OR EXPERIMENTS AND PERMANENT PLANT MODIFICATIONS BASELINE INSPECTION REPORT 05000346/2011009(DRS)
==Dear Mr. Allen:==
On January 27, 2011, the U.S. Nuclear Regulatory Commission (NRC) partially completed an Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications inspection at your Davis-Besse Nuclear Power Station. The inspection hours for this inspection were reduced, such that the remaining inspection hours would be completed during our inspection of your reactor vessel head replacement activities. The enclosed inspection report documents the inspection results, which were discussed on January 27, 2011, with you and other members of your staff.


==Dear Mr. Allen:==
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
On January 27, 2011, the U.S. Nuclear Regulatory Commission (NRC) partially completed an Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications inspection at your Davis-Besse Nuclear Power Station. The inspection hours for this inspection were reduced, such that the remaining inspection hours would be completed during our inspection of your reactor vessel head replacement activities. The enclosed inspection report documents the inspection results, which were discussed on January 27, 2011, with you and other members of your staff. The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.
 
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.


The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of this inspection, no findings of significance were identified.
Based on the results of this inspection, no findings of significance were identified.


In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS) component of NRC's Agencywide Documents Access and Management System (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS) component of NRC's Agencywide Documents Access and Management System (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


Sincerely,/RA/ Robert C. Daley, Chief Engineering Branch 3 Division of Reactor Safety Docket No.: 50-346 License No.: NPF-3  
Sincerely,
/RA/
Robert C. Daley, Chief Engineering Branch 3 Division of Reactor Safety Docket No.: 50-346 License No.: NPF-3


===Enclosure:===
===Enclosure:===
Inspection Report 05000346/2011009(DRS)  
Inspection Report 05000346/2011009(DRS)
w/Attachment: Supplemental Information


===w/Attachment:===
REGION III==
Supplemental Information cc w/encl: Distribution via ListServ Enclosure U. S. NUCLEAR REGULATORY COMMISSION REGION III Docket No.: 50-346 License No.: NPF-3 Report No: 05000346/2011009(DRS) Licensee: FirstEnergy Nuclear Operating Company (FENOC)
Docket No.: 50-346 License No.: NPF-3 Report No: 05000346/2011009(DRS)
Facility: Davis-Besse Nuclear Power Station Location: Oak Harbor, OH Dates: January 10 - 14, 2011, and January 24 - 27, 2011 Inspectors: George M. Hausman, Senior Reactor Inspector (Lead) Ronald A. Langstaff, Senior Reactor Inspector Approved by: Robert C. Daley, Chief Engineering Branch 3 Division of Reactor Safety 1 Enclosure  
Licensee: FirstEnergy Nuclear Operating Company (FENOC)
Facility: Davis-Besse Nuclear Power Station Location: Oak Harbor, OH Dates: January 10 - 14, 2011, and January 24 - 27, 2011 Inspectors: George M. Hausman, Senior Reactor Inspector (Lead)
Ronald A. Langstaff, Senior Reactor Inspector Approved by: Robert C. Daley, Chief Engineering Branch 3 Division of Reactor Safety Enclosure


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
IR 05000346/2011009(DRS); 01/14/2011 - 01/27/2011; Davis-Besse Nuclear Power Station; Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications. This report covers a two-week announced baseline inspection of IP 71111.17, "Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications.The inspection was conducted by Region III based engineering inspectors. The baseline inspection resources were reduced, such that a third of the inspection hours would be completed during performance of IP 71007, "Reactor Vessel Head Replacement Inspection.As a result of this inspection's reduced resources, the baseline inspection program requirements were only partially completed. The remaining required inspection samples and hours shall be completed by the inspectors performing the IP 71007 inspection and will be charged to IP 71111.17 to complete this inspection. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.
IR 05000346/2011009(DRS); 01/14/2011 - 01/27/2011; Davis-Besse Nuclear Power Station;
 
Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications.
 
This report covers a two-week announced baseline inspection of IP 71111.17, Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications. The inspection was conducted by Region III based engineering inspectors. The baseline inspection resources were reduced, such that a third of the inspection hours would be completed during performance of IP 71007, Reactor Vessel Head Replacement Inspection. As a result of this inspections reduced resources, the baseline inspection program requirements were only partially completed. The remaining required inspection samples and hours shall be completed by the inspectors performing the IP 71007 inspection and will be charged to IP 71111.17 to complete this inspection. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.


===A. NRC-Identified===
===NRC-Identified===
and Self-Revealed Findings No findings of significance were identified.
and Self-Revealed Findings No findings of significance were identified.


===B. Licensee-Identified Violations===
===Licensee-Identified Violations===
 
No violations of significance were identified.
No violations of significance were identified.


Line 54: Line 66:
==REACTOR SAFETY==
==REACTOR SAFETY==


===Cornerstone:===
===Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity===
Initiating Events, Mitigating Systems, and Barrier Integrity
{{a|1R17}}
{{a|1R17}}
==1R17 Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications==
==1R17 Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications==
{{IP sample|IP=IP 71111.17}}
{{IP sample|IP=IP 71111.17}}
For this baseline inspection, the hours have been reduced to support the future performance of IP 71007,"Reactor Vessel Head Replacement Inspection.Specifically, the IP 71007 inspection procedure requires that other baseline inspection procedures, such as this inspection, be utilized to credit completion of the IP 71007 inspection. The licensee is currently scheduled to complete their reactor vessel head replacement activities sometime later this year. As a result of this inspection's reduced hours, the baseline inspection program requirements were only partially completed. The remaining required inspection samples (i.e., two evaluations) and inspection hours shall be completed by the inspectors performing the IP 71007 inspection and will be charged to IP 71111.17 to complete this inspection.
For this baseline inspection, the hours have been reduced to support the future performance of IP 71007,Reactor Vessel Head Replacement Inspection. Specifically, the IP 71007 inspection procedure requires that other baseline inspection procedures, such as this inspection, be utilized to credit completion of the IP 71007 inspection. The licensee is currently scheduled to complete their reactor vessel head replacement activities sometime later this year. As a result of this inspections reduced hours, the baseline inspection program requirements were only partially completed. The remaining required inspection samples (i.e., two evaluations) and inspection hours shall be completed by the inspectors performing the IP 71007 inspection and will be charged to IP 71111.17 to complete this inspection.


===.1 Evaluation of Changes, Tests, or Experiments===
===.1 Evaluation of Changes, Tests, or Experiments===
Line 68: Line 79:
* the safety issue requiring the change, tests or experiment was resolved;
* the safety issue requiring the change, tests or experiment was resolved;
* the licensee conclusions for evaluations of changes, tests, or experiments were correct and consistent with 10 CFR 50.59; and
* the licensee conclusions for evaluations of changes, tests, or experiments were correct and consistent with 10 CFR 50.59; and
* the design and licensing basis documentation was updated to reflect the change. The inspectors used, in part, Nuclear Energy Institute (NEI) 96-07, "Guidelines for 10 CFR 50.59 Implementation," Revision 1, to determine acceptability of the completed evaluations, and screenings. The NEI document was endorsed by the NRC in Regulatory Guide 1.187, "Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments," dated November 2000. The inspectors also consulted Part 9900 of the NRC Inspection Manual, "10 CFR Guidance for 10 CFR 50.59, Changes, Tests, and Experiments."
* the design and licensing basis documentation was updated to reflect the change.


3 Enclosure This inspection constituted four samples of evaluations and 14 samples of changes as defined in IP 71111.17-04.
The inspectors used, in part, Nuclear Energy Institute (NEI) 96-07, Guidelines for 10 CFR 50.59 Implementation, Revision 1, to determine acceptability of the completed evaluations, and screenings. The NEI document was endorsed by the NRC in Regulatory Guide 1.187, Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments, dated November 2000. The inspectors also consulted Part 9900 of the NRC Inspection Manual, 10 CFR Guidance for 10 CFR 50.59, Changes, Tests, and Experiments.
 
This inspection constituted four samples of evaluations and 14 samples of changes as defined in IP 71111.17-04.


====b. Findings====
====b. Findings====
Line 83: Line 96:
* the procedures and training plans affected by the modification have been adequately updated;
* the procedures and training plans affected by the modification have been adequately updated;
* the test documentation as required by the applicable test programs has been updated; and
* the test documentation as required by the applicable test programs has been updated; and
* post-modification testing adequately verified system operability and/or functionality. The inspectors also used applicable industry standards to evaluate acceptability of the modifications. The list of modifications and other documents reviewed by the inspectors is included as an Attachment to this report. This inspection constituted seven permanent plant modification samples as defined in IP 71111.17-04.
* post-modification testing adequately verified system operability and/or functionality.
 
The inspectors also used applicable industry standards to evaluate acceptability of the modifications. The list of modifications and other documents reviewed by the inspectors is included as an Attachment to this report.
 
This inspection constituted seven permanent plant modification samples as defined in IP 71111.17-04.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
4 Enclosure


==OTHER ACTIVITIES (OA)==
==OTHER ACTIVITIES (OA)==
Line 101: Line 116:
====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|4OA6}}
{{a|4OA6}}
==4OA6 Meetings==
==4OA6 Meetings==


===.1 Exit Meeting Summary===
===.1 Exit Meeting Summary===
On January 27, 2011, the inspectors presented the inspection results to Mr. B. Allen, and other members of the licensee staff. The licensee personnel acknowledged the inspection results presented and did not identify any proprietary content. The inspectors confirmed that all proprietary material reviewed during the inspection was returned to the licensee staff. ATTACHMENT:
 
On January 27, 2011, the inspectors presented the inspection results to Mr. B. Allen, and other members of the licensee staff. The licensee personnel acknowledged the inspection results presented and did not identify any proprietary content. The inspectors confirmed that all proprietary material reviewed during the inspection was returned to the licensee staff.
 
ATTACHMENT:  


=SUPPLEMENTAL INFORMATION=
=SUPPLEMENTAL INFORMATION=


==KEY POINTS OF CONTACT==
==KEY POINTS OF CONTACT==
Licensee  
 
: [[contact::B. Allen]], Site Vice President - Davis-Besse Nuclear  
Licensee
: [[contact::C. Atkinson]], Advance Nuclear Engineer - Design Engineering (Mechanical/Structural)  
: [[contact::B. Allen]], Site Vice President - Davis-Besse Nuclear
: [[contact::A. Bless]], Electrical Engineer - Design Engineering  
: [[contact::C. Atkinson]], Advance Nuclear Engineer - Design Engineering (Mechanical/Structural)
: [[contact::K. Byrd]], Director - Performance Improvement  
: [[contact::A. Bless]], Electrical Engineer - Design Engineering
: [[contact::J. Cuff]], Manager - Maintenance  
: [[contact::K. Byrd]], Director - Performance Improvement
: [[contact::V. Kaminskas]], Director - Site Engineering  
: [[contact::J. Cuff]], Manager - Maintenance
: [[contact::P. McCloskey]], Manager - Site Regulatory Compliance  
: [[contact::V. Kaminskas]], Director - Site Engineering
: [[contact::M. Murtha]], Staff Engineer - Design Engineering (Electrical/I&C)  
: [[contact::P. McCloskey]], Manager - Site Regulatory Compliance
: [[contact::G. Olson]], Project Manager - Site Projects  
: [[contact::M. Murtha]], Staff Engineer - Design Engineering (Electrical/I&C)
: [[contact::S. Osting]], Supervisor - Design Engineering (Mechanical/Civil)  
: [[contact::G. Olson]], Project Manager - Site Projects
: [[contact::C. Price]], Director - Special Projects  
: [[contact::S. Osting]], Supervisor - Design Engineering (Mechanical/Civil)
: [[contact::J. Tabbert]], Engineer - Procurement Engineering  
: [[contact::C. Price]], Director - Special Projects
: [[contact::V. Wadsworth]], Nuclear Specialist - Regulatory Compliance  
: [[contact::J. Tabbert]], Engineer - Procurement Engineering
: [[contact::G. Wolf]], Supervisor - Regulatory Compliance  
: [[contact::V. Wadsworth]], Nuclear Specialist - Regulatory Compliance
: [[contact::G. Wolf]], Supervisor - Regulatory Compliance
: [[contact::K. Zellers]], Engineering Analysis Supervisor - Design Engineering
: [[contact::K. Zellers]], Engineering Analysis Supervisor - Design Engineering
Nuclear Regulatory Commission
Nuclear Regulatory Commission
: [[contact::J. Rutkowski]], Senior Resident Inspector
: [[contact::J. Rutkowski]], Senior Resident Inspector
 
==LIST OF ITEMS==
==LIST OF ITEMS==
OPENED, CLOSED AND DISCUSSED Opened, Closed, and Discussed None
 
Attachment
===OPENED, CLOSED AND DISCUSSED===
 
===Opened, Closed, and Discussed===
 
None Attachment
 
==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
The following is a list of documents reviewed during the inspection.
 
: Inclusion on this list does not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that selected sections of portions of the documents were evaluated as part of the overall inspection effort.
: Inclusion of a document on this list does not imply NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection report. 10
: CFR 50.59 EVALUATIONS Number Description or TitleDate or Revision 07-00509 Dose Increase Caused by ECCS Leakage Into The Auxiliary Building and BWST, Revision 00 April 12, 2007 07-02986
: DB-OP-02000 - RPS, SFAS, SFRCS Trip or SG Tube Rupture, Revision 20 and Supporting Documents, Revision 00 June 28, 20007 08-00442 36 inch Main Steam Line Break in Room 601 and 602, Revision 00 May 16, 2008 08-03618 Allowable SW Flow Diversion During Cold Weather, Revision 00 November 13, 2008 10
: CFR 50.59 SCREENINGS Number Description or TitleDate or Revision 07-03797 RPS Rx Power Related Field Trip Setpoints, Revision 00 December 19, 200708-01800 Replace RCP Seal Injection Flow Transmitters, Revision 00 August 29, 2008 09-01396 Reroute AFW Common Suction Piping, Revision 05 April 19, 2010 09-04856 TM - Add Boric Acid to
: CFT-2 November 19, 200910-00302 TM - Remove Valve Internals from SW110, Revision 00 February 1, 2010 10-02545 Revise AFW Pump Suction Pressure Switch Setpoint and Tolerance, Revision 00 June 7, 2010 10-04024 TRM Section 8.1.1 Changes, Revision 00 September 27, 201010-04028 TRM Section 8.3.7 Changes, Revision 00 September 27, 201010-04088 TRM Section 8.4.1 Changes, Revision 00 September 27, 201010-04088 TRM Section 8.4.4 Changes, Revision 00 September 27, 201010-04103 TRM Section 8.7.6 and TRM 8.7.6 Bases Changes, Revision 00 September 27, 2010 CALCULATIONS Number Description or Title Date or Revision C-ICE-050.03-003 AFW Low Pressure Suction Setpoint, Revision 1 June 7, 2010 C-ICE-058.01-008 RPS Rx Power Related Field Trip Setpoints, Revision 4 December 20, 2007MPR-3332 Davis-Besse AFW Piping System Modification Analysis, Revision 0 July 2009
: MPR-3373 Evaluation of Davis-Besse Modification
: ECP 08-0571, AFW System Modification, Revision 2 December 2010 
: Attachment
: CORRECTIVE ACTION PROGRAM DOCUMENTS ISSUED DURING INSPECTION Number Description or TitleDate or Revision 11-88717
: NRC 2011, 50.59 Inspection January 25, 2011 11-88784 2011 50.59 Inspection,
: ECP 08-0571-006 Confusing Statement January 25, 2011 11-88850 2011 MOD/50.59 Inspection; Calculation and TRM Discrepancy on Calibration Period January 27, 2011
: CORRECTIVE ACTION PROGRAM DOCUMENTS REVIEWED Number Description or TitleDate or Revision CR08-37919 Contractor Signed 50.59 After Qualification Lapsed April 8, 2008 CR08-42414 NRC MOD/50.59: 50.59 Review May Not Be Complete June 26, 2008
: CR08-47595 10CFR50.59 Review May Not Be Complete October 9, 2008 CR08-48790 50.59 Reviews Performed After Qualifications Expired October 31, 2008 CR10-70203 Matrix Not Updated For 50.59 Review Qualification January 19, 2010
: CR10-76194 MRB Comment Review Condition Identified for Past Operability May 7, 2010 CR10-77485 Individual Signed 50.59 After Qualification Lapsed May 28, 2010
: MODIFICATIONS Number Description or TitleDate or Revision
: ECP 05-0240-00 Replace RCP Seal Injection Flow Transmitters, Revision 00 September 5, 2008ECP 08-0571-006 Replace Low AFW Suction Pressure Switches and Resolve Margin Issue Identified In
: MPR-3332, Revision 0 January 21, 2010
: PART/COMPONENT EQUIVALENT
: REPLACEMENT PACKAGE (PERP) Number Description or TitleDate or Revision 00129 Replace Motor
: DB-MC58, Revision 01 February 6, 2009
: PROCEDURES Number Description or TitleDate or Revision
: DB-OP-02000 RPS, SFAS, SFRCS Trip, or SG Tube Rupture, Procedure Approval Form dated June 29, 2007 20
: DB-OP-06015 BWST Operating Procedure 13 & 14
: NOP-CC-2003 Engineering Changes 15 
: Attachment REFERENCES Number Description or TitleDate or Revision 10
: CFR 50.36 Technical Specifications
: A21672 Commitment Closeout / Extension
: DBE-10-00077 (TSTF - 493) July 6, 2010 M-327AQ-00036 Vendor Manual:
: Rosemount Inc. Instruction Manual for Model 1152 Alphaline Pressure Transmitter for Nuclear Service (Revision BA, April 1, 2007) 5 Notification
: 600625175 Adopt TSTF - 493, Revision 4, Option B July 6, 2010 TRM 8.7.6 TRM AFW System, Technical Verification Requirements 7
: REGULATORY APPLICABILITY DETERMNATIONS (RADs) Number Description or TitleDate or Revision 08-01484 RPS Power Related Setpoint Changes for Measurement Uncertainty Recapture Power Up Rate, Including Addition To TRM, Revision 00 June 3, 2008 08-04589 Replacement Motor for
: DB-MC58, Revision 01 February 6, 2009 09-04014 BWST Operating Procedure, Revision 00 September 25, 2009
: Attachment
==LIST OF ACRONYMS==
: [[USED]] [[]]
: [[ADAMS]] [[Agencywide Documents Access and Management System]]
: [[AFW]] [[Auxiliary Feedwater System]]
: [[BWST]] [[Borated Water Storage Tank]]
: [[CFR]] [[Code of Federal Regulations]]
: [[CFT]] [[Core Flood Tank]]
: [[DRP]] [[Division of Reactor Project]]
: [[DRS]] [[Division of Reactor Safety]]
: [[ECCS]] [[Emergency Core Cooling System]]
: [[ECP]] [[Engineering Change Package FENOC FirstEnergy Nuclear Operating Company]]
: [[I&C]] [[Instrumentation and Control]]
: [[IMC]] [[Inspection Manual Chapter]]
: [[IP]] [[Inspection Procedure]]
: [[IR]] [[Inspection Report]]
: [[MOD]] [[Modification]]
: [[MPR]] [[]]
: [[MPR]] [[Associates]]
: [[MRB]] [[Management Review Board]]
: [[NEI]] [[Nuclear Energy Institute]]
: [[NPF]] [[Nuclear Power Facility]]
: [[NRC]] [[U.S. Nuclear Regulatory Commission]]
: [[NUREG]] [[]]
: [[NRC]] [[Technical Report Designation]]
: [[OA]] [[Other Activities]]
: [[PARS]] [[Public Available Records System]]
: [[PERP]] [[Part/Component Equivalent Replacement Package]]
: [[RCP]] [[Reactor Coolant Pump]]
: [[RPS]] [[Reactor Protection System Rx Reactor]]
: [[SDP]] [[Significance Determination Process]]
: [[SFAS]] [[Safety Features Actuation System]]
: [[SFRCS]] [[Steam and Feed Rupture Control System]]
: [[SG]] [[Steam Generator]]
: [[SW]] [[Service Water]]
: [[TM]] [[Temporary Modification]]
: [[TRM]] [[Technical Requirements Manual]]
: [[TSTF]] [[Technical Specification Task Force]]
: [[B.]] [[Allen    -2- Documents Access and Management System (]]
: [[ADAMS]] [[), accessible from the]]
: [[NRC]] [[Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). Sincerely, /]]
RA/
Robert
: [[C.]] [[Daley, Chief Engineering Branch 3 Division of Reactor Safety Docket No.:  50-346 License No.:]]
: [[NPF]] [[-3 Enclosure: Inspection Report 05000346/2011009(DRS)  w/Attachment:  Supplemental Information cc w/encl: Distribution via ListServ]]
}}
}}

Latest revision as of 10:15, 21 December 2019

IR 05000346-11-009(DRS), on 01/14/2011, 01/27/2011, Davis-Besse Nuclear Power Station; Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications
ML110540503
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 02/22/2011
From: Robert Daley
Engineering Branch 3
To: Allen B
FirstEnergy Nuclear Operating Co
References
IR-11-009
Download: ML110540503 (13)


Text

ary 22, 2011

SUBJECT:

DAVIS-BESSE NUCLEAR POWER STATION, EVALUATIONS OF CHANGES, TESTS, OR EXPERIMENTS AND PERMANENT PLANT MODIFICATIONS BASELINE INSPECTION REPORT 05000346/2011009(DRS)

Dear Mr. Allen:

On January 27, 2011, the U.S. Nuclear Regulatory Commission (NRC) partially completed an Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications inspection at your Davis-Besse Nuclear Power Station. The inspection hours for this inspection were reduced, such that the remaining inspection hours would be completed during our inspection of your reactor vessel head replacement activities. The enclosed inspection report documents the inspection results, which were discussed on January 27, 2011, with you and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the results of this inspection, no findings of significance were identified.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS) component of NRC's Agencywide Documents Access and Management System (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Robert C. Daley, Chief Engineering Branch 3 Division of Reactor Safety Docket No.: 50-346 License No.: NPF-3

Enclosure:

Inspection Report 05000346/2011009(DRS)

w/Attachment: Supplemental Information

REGION III==

Docket No.: 50-346 License No.: NPF-3 Report No: 05000346/2011009(DRS)

Licensee: FirstEnergy Nuclear Operating Company (FENOC)

Facility: Davis-Besse Nuclear Power Station Location: Oak Harbor, OH Dates: January 10 - 14, 2011, and January 24 - 27, 2011 Inspectors: George M. Hausman, Senior Reactor Inspector (Lead)

Ronald A. Langstaff, Senior Reactor Inspector Approved by: Robert C. Daley, Chief Engineering Branch 3 Division of Reactor Safety Enclosure

SUMMARY OF FINDINGS

IR 05000346/2011009(DRS); 01/14/2011 - 01/27/2011; Davis-Besse Nuclear Power Station;

Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications.

This report covers a two-week announced baseline inspection of IP 71111.17, Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications. The inspection was conducted by Region III based engineering inspectors. The baseline inspection resources were reduced, such that a third of the inspection hours would be completed during performance of IP 71007, Reactor Vessel Head Replacement Inspection. As a result of this inspections reduced resources, the baseline inspection program requirements were only partially completed. The remaining required inspection samples and hours shall be completed by the inspectors performing the IP 71007 inspection and will be charged to IP 71111.17 to complete this inspection. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

NRC-Identified

and Self-Revealed Findings No findings of significance were identified.

Licensee-Identified Violations

No violations of significance were identified.

REPORT DETAILS

REACTOR SAFETY

Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity

1R17 Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications

For this baseline inspection, the hours have been reduced to support the future performance of IP 71007,Reactor Vessel Head Replacement Inspection. Specifically, the IP 71007 inspection procedure requires that other baseline inspection procedures, such as this inspection, be utilized to credit completion of the IP 71007 inspection. The licensee is currently scheduled to complete their reactor vessel head replacement activities sometime later this year. As a result of this inspections reduced hours, the baseline inspection program requirements were only partially completed. The remaining required inspection samples (i.e., two evaluations) and inspection hours shall be completed by the inspectors performing the IP 71007 inspection and will be charged to IP 71111.17 to complete this inspection.

.1 Evaluation of Changes, Tests, or Experiments

a. Inspection Scope

From January 10, 2011, through January 27, 2011, the inspectors reviewed four safety evaluations performed pursuant to 10 CFR 50.59 to determine if the evaluations were adequate and that prior NRC approval was obtained as appropriate. The inspectors also reviewed 14 screenings where licensee personnel had determined that a 10 CFR 50.59 evaluation was not necessary. The inspectors reviewed these documents to determine if:

  • the changes, tests, or experiments performed were evaluated in accordance with 10 CFR 50.59 and that sufficient documentation existed to confirm that a license amendment was not required;
  • the safety issue requiring the change, tests or experiment was resolved;
  • the licensee conclusions for evaluations of changes, tests, or experiments were correct and consistent with 10 CFR 50.59; and
  • the design and licensing basis documentation was updated to reflect the change.

The inspectors used, in part, Nuclear Energy Institute (NEI) 96-07, Guidelines for 10 CFR 50.59 Implementation, Revision 1, to determine acceptability of the completed evaluations, and screenings. The NEI document was endorsed by the NRC in Regulatory Guide 1.187, Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments, dated November 2000. The inspectors also consulted Part 9900 of the NRC Inspection Manual, 10 CFR Guidance for 10 CFR 50.59, Changes, Tests, and Experiments.

This inspection constituted four samples of evaluations and 14 samples of changes as defined in IP 71111.17-04.

b. Findings

No findings of significance were identified.

.2 Permanent Plant Modifications

a. Inspection Scope

From January 10, 2011, through January 27, 2011, the inspectors reviewed seven permanent plant modifications that had been installed in the plant during the last three years. This review included in-plant walkdowns for portions of the auxiliary feedwater modification associated with ECP 08-0571 and the Rosemount transmitters modification associated with ECP 05-0240-00. The modifications were selected based upon risk-significance, safety significance, and complexity. The inspectors reviewed the modifications selected to determine if:

  • the supporting design and licensing basis documentation was updated;
  • the changes were in accordance with the specified design requirements;
  • the procedures and training plans affected by the modification have been adequately updated;
  • the test documentation as required by the applicable test programs has been updated; and
  • post-modification testing adequately verified system operability and/or functionality.

The inspectors also used applicable industry standards to evaluate acceptability of the modifications. The list of modifications and other documents reviewed by the inspectors is included as an Attachment to this report.

This inspection constituted seven permanent plant modification samples as defined in IP 71111.17-04.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES (OA)

4OA2 Identification and Resolution of Problems

.1 Routine Review of Condition Reports

a. Inspection Scope

From January 10, 2011, through January 27, 2011, the inspectors reviewed seven corrective action process documents that identified or were related to 10 CFR 50.59 evaluations and permanent plant modifications. The inspectors reviewed these documents to evaluate the effectiveness of corrective actions related to permanent pant modifications and evaluations for changes, tests, or experiments issues. In addition, corrective action documents written on issues identified during the inspection were reviewed to verify adequate problem identification and incorporation of the problems into the corrective action system. The specific corrective action documents that were sampled and reviewed by the inspectors are listed in the attachment to this report.

b. Findings

No findings of significance were identified.

4OA6 Meetings

.1 Exit Meeting Summary

On January 27, 2011, the inspectors presented the inspection results to Mr. B. Allen, and other members of the licensee staff. The licensee personnel acknowledged the inspection results presented and did not identify any proprietary content. The inspectors confirmed that all proprietary material reviewed during the inspection was returned to the licensee staff.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

B. Allen, Site Vice President - Davis-Besse Nuclear
C. Atkinson, Advance Nuclear Engineer - Design Engineering (Mechanical/Structural)
A. Bless, Electrical Engineer - Design Engineering
K. Byrd, Director - Performance Improvement
J. Cuff, Manager - Maintenance
V. Kaminskas, Director - Site Engineering
P. McCloskey, Manager - Site Regulatory Compliance
M. Murtha, Staff Engineer - Design Engineering (Electrical/I&C)
G. Olson, Project Manager - Site Projects
S. Osting, Supervisor - Design Engineering (Mechanical/Civil)
C. Price, Director - Special Projects
J. Tabbert, Engineer - Procurement Engineering
V. Wadsworth, Nuclear Specialist - Regulatory Compliance
G. Wolf, Supervisor - Regulatory Compliance
K. Zellers, Engineering Analysis Supervisor - Design Engineering

Nuclear Regulatory Commission

J. Rutkowski, Senior Resident Inspector

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Opened, Closed, and Discussed

None Attachment

LIST OF DOCUMENTS REVIEWED