IR 05000313/2013003: Difference between revisions

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| issue date = 08/13/2013
| issue date = 08/13/2013
| title = IR 05000313-13-003, 05000368-13-003; 04/01/2013 - 06/30/2013; Arkansas Nuclear One, Units 1 and 2, Integrated Resident and Regional Report; Surveillance Testing, Event Follow-up
| title = IR 05000313-13-003, 05000368-13-003; 04/01/2013 - 06/30/2013; Arkansas Nuclear One, Units 1 and 2, Integrated Resident and Regional Report; Surveillance Testing, Event Follow-up
| author name = Allen D B
| author name = Allen D
| author affiliation = NRC/RGN-IV/DRP/RPB-E
| author affiliation = NRC/RGN-IV/DRP/RPB-E
| addressee name = Browning J
| addressee name = Browning J
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| docket = 05000313, 05000368
| docket = 05000313, 05000368
| license number = DPR-051, NPF-006
| license number = DPR-051, NPF-006
| contact person = Allen D B
| contact person = Allen D
| document report number = IR-13-003
| document report number = IR-13-003
| document type = Inspection Report, Letter
| document type = Inspection Report, Letter
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=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:UNITED STATE S NUC LEAR REGULATOR Y C OMMI SSI ON ust 13, 2013
[[Issue date::August 13, 2013]]


Jeremy Browning, Site Vice President Arkansas Nuclear One Entergy Operations, Inc.
==SUBJECT:==
 
ARKANSAS NUCLEAR ONE - NRC INTEGRATED INSPECTION REPORT 05000313/2013003 AND 05000368/2013003
1448 SR 333 Russellville, AR 72802-0967
 
SUBJECT: ARKANSAS NUCLEAR ONE - NRC INTEGRATED INSPECTION REPORT 05000313/2013003 AND 05000368/2013003


==Dear Mr. Browning:==
==Dear Mr. Browning:==
On June 30, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Arkansas Nuclear One Station Units 1 and 2, facility. The enclosed inspection report documents the inspection results which were discussed on July 2, 2013, with you and other members of your staff.
On June 30, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Arkansas Nuclear One Station Units 1 and 2, facility. The enclosed inspection report documents the inspection results which were discussed on July 2, 2013, with you and other members of your staff.


The inspections examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
The inspections examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.


One NRC identified and one self-revealing finding of very low safety significance (Green) were identified during this inspection. Both of these findings were determined to involve violations of NRC requirements. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
 
One NRC identified and one self-revealing finding of very low safety significance (Green) were identified during this inspection. Both of these findings were determined to involve violations of NRC requirements. The NRC is treating these violations as non-cited violations (NCVs)
consistent with Section 2.3.2.a of the Enforcement Policy.


If you contest these non-cited violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Arkansas Nuclear One.
If you contest these non-cited violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Arkansas Nuclear One.
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In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's Agencywide Document Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's Agencywide Document Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


Sincerely,/RA/
Sincerely,
Donald B. Allen, Chief Project Branch E Division of Reactor Projects Docket Nos.: 05000313, 05000368 License Nos: DPR-51; NPF-6  
/RA/
Donald B. Allen, Chief Project Branch E Division of Reactor Projects Docket Nos.: 05000313, 05000368 License Nos: DPR-51; NPF-6


===Enclosure:===
===Enclosure:===
Inspection Report 05000313/2013003 and 05000368/2013003 w/  
Inspection Report 05000313/2013003 and 05000368/2013003 w/ Attachments: 1. Supplemental Information 2. Request for Information for the Inservice Inspection


===Attachments:===
REGION IV==
1. Supplemental Information 2. Request for Information for the Inservice Inspection cc w/ encl: Electronic Distribution
Docket: 05000313, 05000368 License: DPR-51, NPF-6 Report: 05000313/2013003, 05000368/2013003 Licensee: Entergy Operations Inc.
 
Facility: Arkansas Nuclear One, Units 1 and 2 Location: Junction of Hwy. 64 West and Hwy. 333 South Russellville, Arkansas Dates: April 1 through June 30, 2013 Inspectors: A. Sanchez, Senior Resident Inspector B. Tindell, Senior Resident Inspector A. Fairbanks, Resident Inspector W. Schaup, Resident Inspector R. Azua, Senior Project Engineer I. Anchondo, Senior Reactor Inspector D. Bradley, Project Engineer J. Melfi, Project Engineer Approved By: Don Allen, Chief, Project Branch E Division of Reactor Projects-1-  Enclosure


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
IR 05000313/2013003, 05000368/2013003; 04/01/2013 - 06/30/2013; Arkansas Nuclear One, Units 1 and 2, Integrated Resident and Regional Report; Surveillance Testing, Event Followup. The report covered a 3-month period of inspection by resident inspectors and an announced baseline inspection by region-based inspectors. Two Green non-cited violations were identified.
IR 05000313/2013003, 05000368/2013003; 04/01/2013 - 06/30/2013; Arkansas Nuclear One,
 
Units 1 and 2, Integrated Resident and Regional Report; Surveillance Testing, Event Followup.
 
The report covered a 3-month period of inspection by resident inspectors and an announced baseline inspection by region-based inspectors. Two Green non-cited violations were identified.


The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter 0609, "Significance Determination Process.The cross-cutting aspect is determined using Inspection Manual Chapter 0310, "Components Within the Cross-Cutting Areas.Findings for which the significance determination process does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.
The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter 0609, Significance Determination Process. The cross-cutting aspect is determined using Inspection Manual Chapter 0310, Components Within the Cross-Cutting Areas. Findings for which the significance determination process does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.


===A. NRC-Identified Findings and Self-Revealing Findings===
===NRC-Identified Findings and Self-Revealing Findings===


===Cornerstone: Mitigating Systems===
===Cornerstone: Mitigating Systems===
: '''Green.'''
: '''Green.'''
Inspectors documented a Green self-revealing non-cited violation of Technical Specification 6.4.1.a for the licensee's failure to implement procedures recommended by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.
Inspectors documented a Green self-revealing non-cited violation of Technical Specification 6.4.1.a for the licensees failure to implement procedures recommended by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.


Specifically, the licensee failed to follow procedures for the replacement of the supply breaker for control room emergency chiller 2VE-1A. As a result, the breaker was installed incorrectly and the chiller was inoperable for over two months. Immediate corrective actions included proper installation of the breaker and procedural requirements for visual verification of breaker configuration. The licensee documented the issue in their corrective action program as CR-ANO-2-2013-00233. Inspectors concluded that the failure to follow Procedure 1403.179 for replacement of the train A control room emergency chiller breaker is a performance deficiency. The performance deficiency is more than minor because it was associated with the human performance attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences, and is therefore a finding. Specifically, the loose breaker connection adversely affected the availability and reliability of the control room emergency chiller A. Using Manual Chapter 0609, Attachment 4, "Initial Characterization of Findings," and Appendix A, "The Significance Determination Process (SDP) for Findings at Power," the inspectors determined that the finding required a detailed risk evaluation because it represented an actual loss of function of a single train for longer than its technical specification allowed outage time. The senior reactor analyst performed a detailed risk evaluation using the Arkansas Nuclear One Standardized Plant Analysis Risk models. The dominant risk sequences include a seismically-induced loss of offsite power with the failure of control room emergency chiller A. The analyst assumed that the operators and control room instrumentation could survive a peak control room temperature of 120° F, and that chiller A was susceptible to failure during a seismic event for the 83 days. None of the core damage sequences affected by this performance deficiency were important to the large, early release frequency.
Specifically, the licensee failed to follow procedures for the replacement of the supply breaker for control room emergency chiller 2VE-1A. As a result, the breaker was installed incorrectly and the chiller was inoperable for over two months. Immediate corrective actions included proper installation of the breaker and procedural requirements for visual verification of breaker configuration. The licensee documented the issue in their corrective action program as CR-ANO-2-2013-00233.
 
Inspectors concluded that the failure to follow Procedure 1403.179 for replacement of the train A control room emergency chiller breaker is a performance deficiency.
 
The performance deficiency is more than minor because it was associated with the human performance attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences, and is therefore a finding. Specifically, the loose breaker connection adversely affected the availability and reliability of the control room emergency chiller A. Using Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, and Appendix A, The Significance Determination Process (SDP) for Findings at Power, the inspectors determined that the finding required a detailed risk evaluation because it represented an actual loss of function of a single train for longer than its technical specification allowed outage time. The senior reactor analyst performed a detailed risk evaluation using the Arkansas Nuclear One Standardized Plant Analysis Risk models. The dominant risk sequences include a seismically-induced loss of offsite power with the failure of control room emergency chiller A. The analyst assumed that the operators and control room instrumentation could survive a peak control room temperature of 120° F, and that chiller A was susceptible to failure during a seismic event for the 83 days. None of the core damage sequences affected by this performance deficiency were important to the large, early release frequency.


Therefore, based on the combined internal and seismic ICCDP of 2.9 x 10-7, this finding was of very low safety significance (Green). The finding was determined to have a cross-cutting aspect in the area of human performance, associated with work practices, in that the licensee failed to use work practices that support human performance. Specifically, licensee personnel were aware of the possibility of misaligning the wire grip style lug, but failed to use adequate self and peer checking to ensure the lug was correctly installed [H.4(a)] (Section 4OA3).
Therefore, based on the combined internal and seismic ICCDP of 2.9 x 10-7, this finding was of very low safety significance (Green). The finding was determined to have a cross-cutting aspect in the area of human performance, associated with work practices, in that the licensee failed to use work practices that support human performance. Specifically, licensee personnel were aware of the possibility of misaligning the wire grip style lug, but failed to use adequate self and peer checking to ensure the lug was correctly installed [H.4(a)] (Section 4OA3).
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===Cornerstone: Barrier Integrity===
===Cornerstone: Barrier Integrity===
: '''Green.'''
: '''Green.'''
The inspectors identified a non-cited violation of Unit 2 Technical Specification 6.5.16, "Containment Leakage Rate Testing Program," for the failure to evaluate and take appropriate corrective actions to achieve acceptable performance for containment isolation valves that exceed the local leak rate administrative limit. The licensee entered this issue into the corrective action program as Condition Report CR-ANO-2-2013-01370. The failure to perform a cause determination and take appropriate corrective actions for containment isolation valves that exceed the local leak rate administrative limit was a performance deficiency. The performance deficiency was more than minor because it was associated with the procedure quality attribute of the Barrier Integrity Cornerstone and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events, and is therefore a finding. Specifically, the failure to perform a cause determination and take appropriate corrective actions adversely affected the licensee's ability to ensure containment isolation valves function properly. Using Manual Chapter 0609, Attachment 4, "Initial Characterization of Findings," and Appendix A, "The Significance Determination Process (SDP) for Findings at Power," the finding is determined to have very low safety significance because it did not represent an actual open pathway in the physical integrity of reactor containment, containment isolation system, or heat removal components, and the finding did not involve an actual reduction in function of hydrogen igniters in the reactor containment. Since the cause of the performance deficiency occurred more than three years ago, the inspectors concluded that the finding was not representative of current licensee performance and no cross-cutting aspect was assigned (Section 1R22).
The inspectors identified a non-cited violation of Unit 2 Technical Specification 6.5.16, Containment Leakage Rate Testing Program, for the failure to evaluate and take appropriate corrective actions to achieve acceptable performance for containment isolation valves that exceed the local leak rate administrative limit.
 
The licensee entered this issue into the corrective action program as Condition Report CR-ANO-2-2013-01370.
 
The failure to perform a cause determination and take appropriate corrective actions for containment isolation valves that exceed the local leak rate administrative limit was a performance deficiency. The performance deficiency was more than minor because it was associated with the procedure quality attribute of the Barrier Integrity Cornerstone and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events, and is therefore a finding.
 
Specifically, the failure to perform a cause determination and take appropriate corrective actions adversely affected the licensee's ability to ensure containment isolation valves function properly. Using Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, and Appendix A, The Significance Determination Process (SDP) for Findings at Power, the finding is determined to have very low safety significance because it did not represent an actual open pathway in the physical integrity of reactor containment, containment isolation system, or heat removal components, and the finding did not involve an actual reduction in function of hydrogen igniters in the reactor containment. Since the cause of the performance deficiency occurred more than three years ago, the inspectors concluded that the finding was not representative of current licensee performance and no cross-cutting aspect was assigned (Section 1R22).


===B. Licensee-Identified Violations===
===Licensee-Identified Violations===
None    
 
None
 
=PLANT STATUS=


==PLANT STATUS==
Unit 1 began the period in refueling outage 1R24 and remained shut down for the entire inspection period as the licensee recovered from the main generator stator drop that occurred on March 31, 2013.
Unit 1 began the period in refueling outage 1R24 and remained shut down for the entire inspection period as the licensee recovered from the main generator stator drop that occurred on March 31, 2013.


Unit 2 began the period in a forced outage due to the Unit 1 main generator stator drop. On April 28, 2013, operators performed a reactor startup and closed the main generator output breakers, placing Unit 2 on the grid. Unit 2 reached 100 percent power on April 30, 2013 and remained there for the rest of the period.
Unit 2 began the period in a forced outage due to the Unit 1 main generator stator drop. On April 28, 2013, operators performed a reactor startup and closed the main generator output breakers, placing Unit 2 on the grid. Unit 2 reached 100 percent power on April 30, 2013 and remained there for the rest of the period.


=REPORT DETAILS=
REPORT DETAILS


==REACTOR SAFETY==
==REACTOR SAFETY==
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity {{a|1R01}}
{{a|1R01}}
==1R01 Adverse Weather Protection==
==1R01 Adverse Weather Protection==
{{IP sample|IP=IP 71111.01}}
{{IP sample|IP=IP 71111.01}}
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed a review of preparations for summer weather for selected systems, including conditions that could lead to loss-of-offsite power and conditions that could result from high temperatures. The inspectors reviewed the procedures affecting these areas and the communications protocols between the transmission system operator and the plant to verify that the appropriate information was being exchanged when issues arose that could affect the offsite power system. Examples of aspects considered in the inspectors' review included:
The inspectors performed a review of preparations for summer weather for selected systems, including conditions that could lead to loss-of-offsite power and conditions that could result from high temperatures. The inspectors reviewed the procedures affecting these areas and the communications protocols between the transmission system operator and the plant to verify that the appropriate information was being exchanged when issues arose that could affect the offsite power system. Examples of aspects considered in the inspectors review included:
* The coordination between the transmission system operator and the plant's operations personnel during off-normal or emergency events
* The coordination between the transmission system operator and the plants operations personnel during off-normal or emergency events
* The explanations for the events
* The explanations for the events
* The estimates of when the offsite power system would be returned to a normal state
* The estimates of when the offsite power system would be returned to a normal state
* The notifications from the transmission system operator to the plant when the offsite power system was returned to normal During the inspection, the inspectors focused on plant-specific design features and the procedures used by plant personnel to mitigate or respond to adverse weather conditions. Additionally, the inspectors reviewed the Safety Analysis Report and performance requirements for systems selected for inspection, and verified that operator actions were appropriate as specified by plant-specific procedures. Specific documents reviewed during this inspection are listed in the attachment. The inspectors also reviewed corrective action program items to verify that the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their corrective action program in accordance with station corrective action procedures. The inspectors' reviews focused specifically on the following plant systems:
* The notifications from the transmission system operator to the plant when the offsite power system was returned to normal During the inspection, the inspectors focused on plant-specific design features and the procedures used by plant personnel to mitigate or respond to adverse weather conditions. Additionally, the inspectors reviewed the Safety Analysis Report and performance requirements for systems selected for inspection, and verified that operator actions were appropriate as specified by plant-specific procedures. Specific documents
 
reviewed during this inspection are listed in the attachment. The inspectors also reviewed corrective action program items to verify that the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their corrective action program in accordance with station corrective action procedures. The inspectors reviews focused specifically on the following plant systems:
* Startup transformers
* Startup transformers
* Vital buses
* Vital buses
* Emergency diesel generators These activities constitute completion of one sample to evaluate the readiness of offsite and alternate ac power for summer weather, as defined in Inspection Procedure 71111.01-05.
* Emergency diesel generators These activities constitute completion of one sample to evaluate the readiness of offsite and alternate ac power for summer weather, as defined in Inspection Procedure 71111.01-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R04}}
{{a|1R04}}
==1R04 Equipment Alignment==
==1R04 Equipment Alignment==
{{IP sample|IP=IP 71111.04}}
{{IP sample|IP=IP 71111.04}}
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The inspectors performed partial system walkdowns of the following risk-significant systems:
The inspectors performed partial system walkdowns of the following risk-significant systems:
* June 5, 2013, Unit 2, high pressure safety injection pumps A and C while high pressure safety injection pump B was unavailable for planned maintenance
* June 5, 2013, Unit 2, high pressure safety injection pumps A and C while high pressure safety injection pump B was unavailable for planned maintenance
* June 6, 2013, Unit 1, emergency diesel generator A while emergency diesel generator B was unavailable for planned maintenance The inspectors selected the systems based on their risk significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors focused on any discrepancies that could affect the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, the Safety Analysis Report, technical specification requirements, administrative technical specifications, outstanding work orders, condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also inspected accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program with the appropriate significance characterization. Specific documents reviewed during this inspection are listed in the attachment.
* June 6, 2013, Unit 1, emergency diesel generator A while emergency diesel generator B was unavailable for planned maintenance The inspectors selected the systems based on their risk significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors focused on any discrepancies that could affect the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, the Safety Analysis Report, technical specification requirements, administrative technical specifications, outstanding work orders, condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also inspected accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program with
 
the appropriate significance characterization. Specific documents reviewed during this inspection are listed in the attachment.


These activities constitute completion of two partial system walkdown samples as defined in Inspection Procedure 71111.04-05.
These activities constitute completion of two partial system walkdown samples as defined in Inspection Procedure 71111.04-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R05}}
{{a|1R05}}
==1R05 Fire Protection==
==1R05 Fire Protection==
{{IP sample|IP=IP 71111.05}}
{{IP sample|IP=IP 71111.05}}
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* June 25, 2013, Unit 2, Fire Zone 2098-L, cable spreading room
* June 25, 2013, Unit 2, Fire Zone 2098-L, cable spreading room
* June 25, 2013, Unit 2, Fire Zone NA, intake structure
* June 25, 2013, Unit 2, Fire Zone NA, intake structure
* June 26, 2013, Unit 1, Fire Zone 170-Z, steam pipe area The inspectors reviewed areas to assess if licensee personnel had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant; effectively maintained fire detection and suppression capability; maintained passive fire protection features in good material condition; and had implemented adequate compensatory measures for out of service, degraded or inoperable fire protection equipment, systems, or features, in accordance with the licensee's fire plan.
* June 26, 2013, Unit 1, Fire Zone 170-Z, steam pipe area The inspectors reviewed areas to assess if licensee personnel had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant; effectively maintained fire detection and suppression capability; maintained passive fire protection features in good material condition; and had implemented adequate compensatory measures for out of service, degraded or inoperable fire protection equipment, systems, or features, in accordance with the licensees fire plan.


The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plant's individual plant examination of external events with later additional insights, their potential to affect equipment that could initiate or mitigate a plant transient, or their impact on the plant's ability to respond to a security event. Using the documents listed in the attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. Specific documents reviewed during this inspection are listed in the attachment.
The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants individual plant examination of external events with later additional insights, their potential to affect equipment that could initiate or mitigate a plant transient, or their impact on the plants ability to respond to a security event. Using the documents listed in the attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. Specific documents reviewed during this inspection are listed in the attachment.


These activities constitute completion of four quarterly fire-protection inspection samples as defined in Inspection Procedure 71111.05-05.
These activities constitute completion of four quarterly fire-protection inspection samples as defined in Inspection Procedure 71111.05-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R06}}
{{a|R06}}
==1R06 Flood Protection Measures==
==R06 Flood Protection Measures==
{{IP sample|IP=IP 71111.06}}
{{IP sample|IP=IP 71111.06}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the Safety Analysis Report, the flooding analysis, and plant procedures to assess susceptibilities involving internal flooding; reviewed the corrective action program to determine if licensee personnel identified and corrected flooding problems; and verified that operator actions for coping with flooding can reasonably achieve the desired outcomes. The inspectors also inspected the areas listed below to verify the adequacy of equipment seals located below the flood line, floor and wall penetration seals, watertight door seals, common drain lines and sumps, sump pumps, level alarms, and control circuits, and temporary or removable flood barriers. Specific documents reviewed during this inspection are listed in the attachment.
The inspectors reviewed the Safety Analysis Report, the flooding analysis, and plant procedures to assess susceptibilities involving internal flooding; reviewed the corrective action program to determine if licensee personnel identified and corrected flooding problems; and verified that operator actions for coping with flooding can reasonably achieve the desired outcomes. The inspectors also inspected the areas listed below to verify the adequacy of equipment seals located below the flood line, floor and wall penetration seals, watertight door seals, common drain lines and sumps, sump pumps, level alarms, and control circuits, and temporary or removable flood barriers. Specific documents reviewed during this inspection are listed in the attachment.
* May 24, 2013, Units 1 and 2, intake structures, 366 foot level These activities constitute completion of one flood protection measures inspection sample as defined in Inspection Procedure 71111.06-05.
* May 24, 2013, Units 1 and 2, intake structures, 366 foot level These activities constitute completion of one flood protection measures inspection sample as defined in Inspection Procedure 71111.06-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R08}}
{{a|1R08}}
==1R08 Inservice Inspection Activities==
==1R08 Inservice Inspection Activities==
{{IP sample|IP=IP 71111.08}}
{{IP sample|IP=IP 71111.08}}
Completion of Sections
Completion of Sections


===.1 through .5, below, constitutes completion of one sample as defined in Inspection Procedure 71111.08-05. .1 Inspection Activities Other Than Steam Generator Tube Inspection, Pressurized Water Reactor Vessel Upper Head Penetration Inspections, and Boric Acid Corrosion Control (71111.08-02.01)===
===.1 through .5, below, constitutes completion of one sample as===
 
defined in Inspection Procedure 71111.08-05.
 
===.1 Inspection Activities Other Than Steam Generator Tube Inspection, Pressurized Water===
 
Reactor Vessel Upper Head Penetration Inspections, and Boric Acid Corrosion Control       (71111.08-02.01)


====a. Inspection Scope====
====a. Inspection Scope====
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The inspectors directly observed the following nondestructive examinations:
The inspectors directly observed the following nondestructive examinations:
SYSTEM WELD IDENTIFICATION EXAMINATION         TYPE Reactor Coolant System Pressurizer Relief Nozzle Between W-X Axis (Report No. 1-ISI-UT-13-017) Ultrasonic SYSTEM WELD IDENTIFICATION EXAMINATION         TYPE Reactor Coolant System  Cold Leg Drain Nozzle to SE Circ Weld (Report No. 1-ISI-UT-13-020) Ultrasonic Main Steam EBB-3-MS-143, I.W.A (Report No. 1-ISI-MT-13-001) Magnetic Particle  Building Spray HCD-8/BS-123 (Report No. 1-ISI-VT-13-042) Visual (VT-3)  The inspectors reviewed records for the following nondestructive examinations:
SYSTEM             WELD IDENTIFICATION                       EXAMINATION TYPE Reactor Coolant     Pressurizer Relief Nozzle                 Ultrasonic System              Between W-X Axis (Report No. 1-ISI-UT-13-017)
SYSTEM WELD IDENTIFICATION EXAMINATION         TYPE Reactor Coolant System Pipe-to-pipe weld (Report No. 1-ISI-UT-13-021) Ultrasonic Reactor Coolant System Pipe-to-Cap weld (Report No.1-BOP-RT-13-011) Radiographic Reactor Coolant System Reducer-to-Flange weld (Report No.1-BOP-RT-13-0070) Radiographic Reactor Coolant System Pipe-to-elbow weld (Report No. 1-BOP-RT-13-012) Radiographic  During the review and observation of each examination, the inspectors verified that activities were performed in accordance with the American Society of Mechanical Engineers (ASME) code requirements and applicable procedures. The inspectors also verified the qualifications of all nondestructive examination technicians performing the inspections were current.
 
SYSTEM               WELD IDENTIFICATION                       EXAMINATION TYPE Reactor Coolant     Cold Leg Drain Nozzle to SE Circ Weld     Ultrasonic System              (Report No. 1-ISI-UT-13-020)
Main Steam           EBB-3-MS-143, I.W.A                       Magnetic Particle (Report No. 1-ISI-MT-13-001)
Building Spray       HCD-8/BS-123                               Visual (VT-3)
                            (Report No. 1-ISI-VT-13-042)
The inspectors reviewed records for the following nondestructive examinations:
SYSTEM                   WELD IDENTIFICATION                   EXAMINATION TYPE Reactor Coolant         Pipe-to-pipe weld                     Ultrasonic System                  (Report No. 1-ISI-UT-13-021)
Reactor Coolant         Pipe-to-Cap weld                       Radiographic System                  (Report No.1-BOP-RT-13-011)
Reactor Coolant         Reducer-to-Flange weld                 Radiographic System                  (Report No.1-BOP-RT-13-0070)
Reactor Coolant         Pipe-to-elbow weld                     Radiographic System                  (Report No. 1-BOP-RT-13-012)
During the review and observation of each examination, the inspectors verified that activities were performed in accordance with the American Society of Mechanical Engineers (ASME) code requirements and applicable procedures. The inspectors also verified the qualifications of all nondestructive examination technicians performing the inspections were current.


These actions constitute completion of the requirements for Section 02.01.
These actions constitute completion of the requirements for Section 02.01.
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated the implementation of the licensee's boric acid corrosion control program for monitoring degradation of those systems that could be adversely affected by boric acid corrosion. The inspectors reviewed the documentation associated with the licensee's boric acid corrosion control walkdown as specified in Procedures SEP-BAC-ANO-001, "Boric Acid Corrosion Control Program Inspection and Identification of Boric Acid Leaks for ANO-1 and ANO-2," Revision 0, CEP-BAC-001, "Boric Acid Corrosion Control (BACC) Program Plan," Revision 0, and EN-DC-319, "Inspection and Evaluation of Boric Acid Leaks," Revision 8. The inspectors also reviewed the visual records of the components and equipment. The inspectors verified that the visual inspections emphasized locations where boric acid leaks could cause degradation of safety-significant components. The inspectors also verified that the engineering evaluations for those components where boric acid was identified gave assurance that the ASME code wall thickness limits were properly maintained. The inspectors confirmed that the corrective actions performed for evidence of boric acid leaks were consistent with requirements of the ASME code. Specific documents reviewed during this inspection are listed in the attachment.
The inspectors evaluated the implementation of the licensees boric acid corrosion control program for monitoring degradation of those systems that could be adversely affected by boric acid corrosion. The inspectors reviewed the documentation associated with the licensees boric acid corrosion control walkdown as specified in Procedures SEP-BAC-ANO-001, Boric Acid Corrosion Control Program Inspection and Identification of Boric Acid Leaks for ANO-1 and ANO-2, Revision 0, CEP-BAC-001, Boric Acid Corrosion Control (BACC) Program Plan, Revision 0, and EN-DC-319, Inspection and Evaluation of Boric Acid Leaks, Revision 8. The inspectors also reviewed the visual records of the components and equipment. The inspectors verified that the visual inspections emphasized locations where boric acid leaks could cause degradation of safety-significant components. The inspectors also verified that the engineering evaluations for those components where boric acid was identified gave assurance that the ASME code wall thickness limits were properly maintained. The inspectors confirmed that the corrective actions performed for evidence of boric acid leaks were consistent with requirements of the ASME code. Specific documents reviewed during this inspection are listed in the attachment.


These actions constitute completion of the requirements for Section 02.03.
These actions constitute completion of the requirements for Section 02.03.
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====a. Inspection Scope====
====a. Inspection Scope====
The licensee performed steam generator inspection activities during refueling outage 1R24 to determine the extent of bowing and tube-to-tube wear progression. The activities were not technical specification required inspections. The scope of the licensee's eddy current testing included:
The licensee performed steam generator inspection activities during refueling outage 1R24 to determine the extent of bowing and tube-to-tube wear progression.
 
The activities were not technical specification required inspections. The scope of the licensees eddy current testing included:
* Bobbin testing of 454 tubes in steam generator A from tube support 09S to upper tube end.
* Bobbin testing of 454 tubes in steam generator A from tube support 09S to upper tube end.
* Bobbin testing of 446 tubes in steam generator B from tube support 09S to upper tube end.
* Bobbin testing of 446 tubes in steam generator B from tube support 09S to upper tube end.
Line 187: Line 222:
* Full length eddy current array probe (X-probe) of 74 tubes in steam generator B exhibiting tube-to-tube wear.
* Full length eddy current array probe (X-probe) of 74 tubes in steam generator B exhibiting tube-to-tube wear.
* Full length eddy current array probe (X-probe) of 51 tubes in steam generator A with prior proximity signals (PRX).
* Full length eddy current array probe (X-probe) of 51 tubes in steam generator A with prior proximity signals (PRX).
* Full length eddy current array probe (X-probe) of 17 tubes in steam generator B with prior proximity signals (PRX). The following tube degradation mechanisms were identified:
* Full length eddy current array probe (X-probe) of 17 tubes in steam generator B with prior proximity signals (PRX).
 
The following tube degradation mechanisms were identified:
* Wear at the tube support plate intersections.
* Wear at the tube support plate intersections.
* Tube-to-tube wear.
* Tube-to-tube wear.
* Tie rods bowing At the conclusion of the eddy current testing, the licensee preventively plugged and stabilized seven tubes in steam generator A and nine tubes in steam generator B.
* Tie rods bowing At the conclusion of the eddy current testing, the licensee preventively plugged and stabilized seven tubes in steam generator A and nine tubes in steam generator B.


The inspectors observed portions of the eddy current testing being performed and verified that: (1) the appropriate probes were used for identifying the expected types of degradation, (2) calibration requirements were adhered to, and (3) probe travel speed was in accordance with procedural requirements. The inspectors performed a review of the site-specific qualifications for the techniques being used, and verified that eddy current test data analyses were adequately performed per Electric Power Research Institute and site specific guidelines.
The inspectors observed portions of the eddy current testing being performed and verified that:
: (1) the appropriate probes were used for identifying the expected types of degradation,
: (2) calibration requirements were adhered to, and
: (3) probe travel speed was in accordance with procedural requirements. The inspectors performed a review of the site-specific qualifications for the techniques being used, and verified that eddy current test data analyses were adequately performed per Electric Power Research Institute and site specific guidelines.


Finally, the inspectors review selected eddy current test data and verified that the analytical techniques used were adequate.
Finally, the inspectors review selected eddy current test data and verified that the analytical techniques used were adequate.
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====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R11}}
{{a|1R11}}
==1R11 Licensed Operator Requalification Program and Licensed Operator Performance==
==1R11 Licensed Operator Requalification Program and Licensed Operator Performance==
{{IP sample|IP=IP 71111.11}}
{{IP sample|IP=IP 71111.11}}
Line 219: Line 258:
* Licensed operator performance
* Licensed operator performance
* The ability of the licensee to administer the evaluations
* The ability of the licensee to administer the evaluations
* Follow-up actions taken by the licensee for identified discrepancies These activities constitute completion of two quarterly licensed operator requalification program samples as defined in Inspection Procedure 71111.11.
* Follow-up actions taken by the licensee for identified discrepancies These activities constitute completion of two quarterly licensed operator requalification program samples as defined in Inspection Procedure 71111.11.


====b. Findings====
====b. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed the performance of on-shift licensed operators in the plant's main control room. The inspectors assessed the operators' adherence to plant procedures, including conduct of operations procedures and other operations department policies. The inspectors observed the operators' performance during the following periods of heightened activities:
The inspectors observed the performance of on-shift licensed operators in the plants main control room. The inspectors assessed the operators adherence to plant procedures, including conduct of operations procedures and other operations
 
department policies. The inspectors observed the operators performance during the following periods of heightened activities:
* April 28, 2013, Unit 2, reactor startup
* April 28, 2013, Unit 2, reactor startup
* June 18, 2013, Unit 1, train B undervoltage surveillances These activities constitute completion of two quarterly licensed operator performance samples as defined in Inspection Procedure 71111.11-05.
* June 18, 2013, Unit 1, train B undervoltage surveillances These activities constitute completion of two quarterly licensed operator performance samples as defined in Inspection Procedure 71111.11-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R12}}
{{a|1R12}}
==1R12 Maintenance Effectiveness==
==1R12 Maintenance Effectiveness==
{{IP sample|IP=IP 71111.12}}
{{IP sample|IP=IP 71111.12}}
Line 249: Line 289:
* Ensuring proper classification in accordance with 10 CFR 50.65(a)(1) or (a)(2)
* Ensuring proper classification in accordance with 10 CFR 50.65(a)(1) or (a)(2)
* Establishing appropriate performance criteria
* Establishing appropriate performance criteria
* Establishing appropriate and adequate goals and corrective actions The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the corrective action program with the appropriate significance characterization. Specific documents reviewed during this inspection are listed in the attachment.
* Establishing appropriate and adequate goals and corrective actions The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the corrective action program with the appropriate significance characterization. Specific documents reviewed during this inspection are listed in the attachment.


These activities constitute completion of two maintenance effectiveness samples as defined in Inspection Procedure 71111.12-05.
These activities constitute completion of two maintenance effectiveness samples as defined in Inspection Procedure 71111.12-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R13}}
{{a|1R13}}
==1R13 Maintenance Risk Assessments and Emergent Work Control==
==1R13 Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13}}
{{IP sample|IP=IP 71111.13}}
Line 267: Line 306:
* April 23, 2013, Unit 1, outage activities following the main generator stator drop
* April 23, 2013, Unit 1, outage activities following the main generator stator drop
* May 4, 2013, Units 1 and 2, dropped stator and damaged carriage removal
* May 4, 2013, Units 1 and 2, dropped stator and damaged carriage removal
* May 20, 2013, Units 1 and 2, heavy equipment in train bay The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4) and that the assessments were accurate and complete. When licensee personnel performed emergent work, the inspectors verified that the licensee personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed the technical specification requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Specific documents reviewed during this inspection are listed in the attachment.
* May 20, 2013, Units 1 and 2, heavy equipment in train bay The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)and that the assessments were accurate and complete. When licensee personnel performed emergent work, the inspectors verified that the licensee personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed the technical specification requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Specific documents reviewed during this inspection are listed in the attachment.


These activities constitute completion of seven maintenance risk assessments and emergent work control inspection samples as defined in Inspection Procedure 71111.13-05.
These activities constitute completion of seven maintenance risk assessments and emergent work control inspection samples as defined in Inspection Procedure 71111.13-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R15}}
{{a|R15}}
==1R15 Operability Evaluations and Functionality Assessments==
==R15 Operability Evaluations and Functionality Assessments==
{{IP sample|IP=IP 71111.15}}
{{IP sample|IP=IP 71111.15}}


Line 284: Line 322:
* April 24, 2013, Unit 2, debris identified in containment during closeout
* April 24, 2013, Unit 2, debris identified in containment during closeout
* May 17, 2013, Unit 1, emergency diesel generator A fretting wear on the turbocharger inlet air turning box north-side support legs
* May 17, 2013, Unit 1, emergency diesel generator A fretting wear on the turbocharger inlet air turning box north-side support legs
* June 7, 2013, Unit 2, wetting of emergency diesel generator B fuel oil transfer pump The inspectors selected these operability and functionality issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure technical specification operability was properly justified and to verify the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the technical specifications and Safety Analysis Report to the licensee's evaluations to determine whether the components or systems were operable or functional. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. Additionally, the inspectors reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Specific documents reviewed during this inspection are listed in the attachment.
* June 7, 2013, Unit 2, wetting of emergency diesel generator B fuel oil transfer pump The inspectors selected these operability and functionality issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure technical specification operability was properly justified and to verify the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the technical specifications and Safety Analysis Report to the licensees evaluations to determine whether the components or systems were operable or functional. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. Additionally, the inspectors reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Specific documents reviewed during this inspection are listed in the attachment.


These activities constitute completion of six operability evaluations inspection samples as defined in Inspection Procedure 71111.15-05.
These activities constitute completion of six operability evaluations inspection samples as defined in Inspection Procedure 71111.15-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R18}}
{{a|R18}}
==1R18 Plant Modifications==
==R18 Plant Modifications==
{{IP sample|IP=IP 71111.18}}
{{IP sample|IP=IP 71111.18}}
Temporary Modifications
Temporary Modifications
Line 299: Line 336:
* April 23, 2013, Unit 1, source range nuclear instrument NI-501 modification for fuel movement
* April 23, 2013, Unit 1, source range nuclear instrument NI-501 modification for fuel movement
* April 15, 2013, Unit 1, startup transformer 1 temporary power supply to vital buses A3 and A4
* April 15, 2013, Unit 1, startup transformer 1 temporary power supply to vital buses A3 and A4
* April 15, 2013, Unit 1, startup transformer 2 temporary power supply to vital buses A3 and A4 buses through temporary switchgear The inspectors reviewed the temporary modifications and the associated safety-evaluation screening against the system design bases documentation, including the Safety Analysis Report and the technical specifications, and verified that the modification did not adversely affect the system operability or availability. The inspectors also verified that the installation and restoration were consistent with the modification documents and that configuration control was adequate. Additionally, the inspectors verified that the temporary modification was identified on control room drawings, appropriate tags were placed on the affected equipment, and licensee personnel evaluated the combined effects on mitigating systems and the integrity of radiological barriers. Specific documents reviewed during this inspection are listed in the attachment. These activities constitute completion of three samples for temporary plant modifications, as defined in Inspection Procedure 71111.18-05.
* April 15, 2013, Unit 1, startup transformer 2 temporary power supply to vital buses A3 and A4 buses through temporary switchgear The inspectors reviewed the temporary modifications and the associated safety-evaluation screening against the system design bases documentation, including the Safety Analysis Report and the technical specifications, and verified that the modification did not adversely affect the system operability or availability. The inspectors also verified that the installation and restoration were consistent with the modification documents and that configuration control was adequate. Additionally, the inspectors verified that the temporary modification was identified on control room drawings, appropriate tags were placed on the affected equipment, and licensee personnel evaluated the combined effects on mitigating systems and the integrity of radiological barriers. Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of three samples for temporary plant modifications, as defined in Inspection Procedure 71111.18-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R19}}
{{a|1R19}}
==1R19 Post-Maintenance Testing==
==1R19 Post-Maintenance Testing==
{{IP sample|IP=IP 71111.19}}
{{IP sample|IP=IP 71111.19}}
Line 313: Line 351:
* June 13, 2013, Unit 1, P-35A, reactor building spray pump A , following bearing and seal replacement
* June 13, 2013, Unit 1, P-35A, reactor building spray pump A , following bearing and seal replacement
* June 14, 2013, Unit 1, K-4B, emergency diesel generator B , following generator bearing replacement
* June 14, 2013, Unit 1, K-4B, emergency diesel generator B , following generator bearing replacement
* April 23, 2013, Alternate AC Diesel Generator Bus 2A9 and the Alternate AC Diesel Generator Following Repairs from the Unit 1 Dropped Stator Event The inspectors selected these activities based upon the structure, system, or component's ability to affect risk. The inspectors evaluated these activities to verify that the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; and test instrumentation was appropriate.
* April 23, 2013, Alternate AC Diesel Generator Bus 2A9 and the Alternate AC Diesel Generator Following Repairs from the Unit 1 Dropped Stator Event The inspectors selected these activities based upon the structure, system, or component's ability to affect risk. The inspectors evaluated these activities to verify that the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; and test instrumentation was appropriate.


The inspectors evaluated the activities against the technical specifications, the Safety Analysis Report, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with post-maintenance tests to determine whether the licensee was identifying problems and entering them in the corrective action program and that the problems were being corrected commensurate with their importance to safety. Specific documents reviewed during this inspection are listed in the attachment. These activities constitute completion of five post-maintenance testing inspection samples as defined in Inspection Procedure 71111.19-05.
The inspectors evaluated the activities against the technical specifications, the Safety Analysis Report, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with post-maintenance tests to determine whether the licensee was identifying problems and entering them in the corrective action program and that the problems were being corrected commensurate with their importance to safety. Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of five post-maintenance testing inspection samples as defined in Inspection Procedure 71111.19-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R20}}
{{a|1R20}}
==1R20 Refueling and Other Outage Activities==
==1R20 Refueling and Other Outage Activities==
{{IP sample|IP=IP 71111.20}}
{{IP sample|IP=IP 71111.20}}
Line 337: Line 376:
* Refueling activities, including fuel handling
* Refueling activities, including fuel handling
* Startup and ascension to full power operation, tracking of startup prerequisites, walkdown of the containment to verify that debris had not been left which could block emergency core cooling system suction strainers
* Startup and ascension to full power operation, tracking of startup prerequisites, walkdown of the containment to verify that debris had not been left which could block emergency core cooling system suction strainers
* Licensee identification and resolution of problems related to refueling outage activities Specific documents reviewed during this inspection are listed in the attachment. These activities constitute completion of one refueling outage and one other outage inspection samples, as defined in Inspection Procedure 71111.20-05.
* Licensee identification and resolution of problems related to refueling outage activities Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of one refueling outage and one other outage inspection samples, as defined in Inspection Procedure 71111.20-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R22}}
{{a|R22}}
==1R22 Surveillance Testing==
==R22 Surveillance Testing==
{{IP sample|IP=IP 71111.22}}
{{IP sample|IP=IP 71111.22}}


Line 361: Line 401:
* Engineering evaluations and root causes
* Engineering evaluations and root causes
* Reference setting data
* Reference setting data
* Annunciators and alarms setpoints The inspectors also verified that licensee personnel identified and implemented any needed corrective actions associated with the surveillance testing.
* Annunciators and alarms setpoints The inspectors also verified that licensee personnel identified and implemented any needed corrective actions associated with the surveillance testing.
* September 24, 2012, Unit 2, letdown isolation valve 2CV-4832-2 local leak rate test
* September 24, 2012, Unit 2, letdown isolation valve 2CV-4832-2 local leak rate test
* February 10, 2013, Units 1 and 2, alternate ac diesel generator quarterly test
* February 10, 2013, Units 1 and 2, alternate ac diesel generator quarterly test
* May 1, 2013, Unit 2, remote pressurizer proportional heater test
* May 1, 2013, Unit 2, remote pressurizer proportional heater test
* May 22, 2013, Unit 2, emergency feedwater pump A inservice test
* May 22, 2013, Unit 2, emergency feedwater pump A inservice test
* May 29, 2013, Unit 2, emergency diesel generator A monthly test Specific documents reviewed during this inspection are listed in the attachment.
* May 29, 2013, Unit 2, emergency diesel generator A monthly test Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of five surveillance testing inspection samples (one pump or valve inservice test sample, one containment isolation valve test sample,


These activities constitute completion of five surveillance testing inspection samples (one pump or valve inservice test sample, one containment isolation valve test sample, and three routine surveillance testing samples) as defined in Inspection Procedure 71111.22-05.
and three routine surveillance testing samples) as defined in Inspection Procedure 71111.22-05.


====b. Findings====
====b. Findings====


=====Introduction.=====
=====Introduction.=====
The inspectors identified a Green non-cited violation of Unit 2 Technical Specification 6.5.16, "Containment Leakage Rate Testing Program," for the failure to evaluate and take appropriate corrective actions to achieve acceptable performance for containment isolation valves that exceed the local leak rate administrative limit.
The inspectors identified a Green non-cited violation of Unit 2 Technical Specification 6.5.16, Containment Leakage Rate Testing Program, for the failure to evaluate and take appropriate corrective actions to achieve acceptable performance for containment isolation valves that exceed the local leak rate administrative limit.


=====Description.=====
=====Description.=====
Line 380: Line 422:
Work was scheduled to be performed on the air operator for the valve; however, no valve seat work was planned or performed. On March 11, 2011, after completion of work on the air operator, the valve exceeded the local leak rate administrative limit. The licensee generated a condition report that was closed to the work order process without a cause evaluation or corrective actions. On September 24, 2012, the valve again exceeded the as-found local leak rate administrative limit, which was documented in CR-ANO-2-2012-02270. The response stated that there were no programmatic requirements and no technical specification implications relative to containment integrity and/or leakage as a result of the leakage from valve 2CV-4823-2 exceeding its administrative limit; therefore, the leak rate from valve 2CV-4823-2 was acceptable. The inspectors noted that the valve was scheduled for repair in the spring of 2014.
Work was scheduled to be performed on the air operator for the valve; however, no valve seat work was planned or performed. On March 11, 2011, after completion of work on the air operator, the valve exceeded the local leak rate administrative limit. The licensee generated a condition report that was closed to the work order process without a cause evaluation or corrective actions. On September 24, 2012, the valve again exceeded the as-found local leak rate administrative limit, which was documented in CR-ANO-2-2012-02270. The response stated that there were no programmatic requirements and no technical specification implications relative to containment integrity and/or leakage as a result of the leakage from valve 2CV-4823-2 exceeding its administrative limit; therefore, the leak rate from valve 2CV-4823-2 was acceptable. The inspectors noted that the valve was scheduled for repair in the spring of 2014.


The inspectors independently reviewed Unit 2 Technical Specification 6.5.16, "Containment Leakage Rate Testing Program" and determined that the licensee's program is required to implement Nuclear Energy Institute 94-01, "Industry Guideline for Implementing Performance-Based Option of 10 CFR Part 50, Appendix J," Revision 2-A. The standard states, in part, that a cause determination should be performed and corrective actions identified that focus on those activities that can eliminate the identified cause of a failure with appropriate steps to eliminate recurrence. A failure, as defined by the standard, is exceeding an administrative limit and not the total failure of the valve. The inspectors reviewed the licensee's corrective action program documents and their containment leakage rate testing program documents, and determined that they did not meet the technical specification required guidance. Specifically, the licensee's programs did not specify that a cause determination be performed for conditions where containment isolation valves exceed their administrative limits. In addition, there was no guidance to ensure that corrective actions address the cause of the failure. The inspectors also noted that the licensee was not treating these items as degraded conditions to ensure that they were corrected in a timely manner. Based on the above and the licensee's statements that the leakage from 2CF-4823-2 was acceptable, the inspectors concluded that the licensee had not adequately implemented Nuclear Energy Institute 94-01, as required by Technical Specification 6.5.16. The inspectors concluded that because the licensee's program was established more than three years ago, the failure to adequately implement the guidance was not representative of current licensee performance.
The inspectors independently reviewed Unit 2 Technical Specification 6.5.16, Containment Leakage Rate Testing Program and determined that the licensees program is required to implement Nuclear Energy Institute 94-01, Industry Guideline for Implementing Performance-Based Option of 10 CFR Part 50, Appendix J, Revision 2-A.
 
The standard states, in part, that a cause determination should be performed and corrective actions identified that focus on those activities that can eliminate the identified cause of a failure with appropriate steps to eliminate recurrence. A failure, as defined by the standard, is exceeding an administrative limit and not the total failure of the valve.
 
The inspectors reviewed the licensees corrective action program documents and their containment leakage rate testing program documents, and determined that they did not meet the technical specification required guidance. Specifically, the licensees programs did not specify that a cause determination be performed for conditions where containment isolation valves exceed their administrative limits. In addition, there was no guidance to ensure that corrective actions address the cause of the failure. The inspectors also noted that the licensee was not treating these items as degraded conditions to ensure that they were corrected in a timely manner. Based on the above and the licensees statements that the leakage from 2CF-4823-2 was acceptable, the inspectors concluded that the licensee had not adequately implemented Nuclear Energy Institute 94-01, as required by Technical Specification 6.5.16.
 
The inspectors concluded that because the licensees program was established more than three years ago, the failure to adequately implement the guidance was not representative of current licensee performance.


=====Analysis.=====
=====Analysis.=====
The failure to perform a cause determination and take appropriate corrective actions for containment isolation valves that exceed the local leak rate administrative limit is a performance deficiency. The performance deficiency is more than minor because it was associated with the procedure quality attribute of the Barrier Integrity Cornerstone and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events, and is therefore a finding. Specifically, the failure to perform a cause determination and take appropriate corrective actions adversely affected the licensee's ability to ensure containment isolation valves function properly.
The failure to perform a cause determination and take appropriate corrective actions for containment isolation valves that exceed the local leak rate administrative limit is a performance deficiency. The performance deficiency is more than minor because it was associated with the procedure quality attribute of the Barrier Integrity Cornerstone and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events, and is therefore a finding. Specifically, the failure to perform a cause determination and take appropriate corrective actions adversely affected the licensee's ability to ensure containment isolation valves function properly.


Using Manual Chapter 0609, Attachment 4, "Initial Characterization of Findings," and Appendix A, "The Significance Determination Process (SDP) for Findings at Power," the finding is determined to have very low safety significance because it did not represent an actual open pathway in the physical integrity of reactor containment, containment isolation system, or heat removal components, and the finding did not involve an actual reduction in function of hydrogen igniters in the reactor containment. Since the cause of the performance deficiency occurred more than three years ago, the inspectors concluded that the finding was not representative of current licensee performance and no cross-cutting aspect was assigned.
Using Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, and Appendix A, The Significance Determination Process (SDP) for Findings at Power, the finding is determined to have very low safety significance because it did not represent an actual open pathway in the physical integrity of reactor containment, containment isolation system, or heat removal components, and the finding did not involve an actual reduction in function of hydrogen igniters in the reactor containment. Since the cause of the performance deficiency occurred more than three years ago, the inspectors concluded that the finding was not representative of current licensee performance and no cross-cutting aspect was assigned.


=====Enforcement.=====
=====Enforcement.=====
Unit 2 Technical Specification 6.5.16, "Containment Leakage Rate Testing Program," states, in part, that a program shall be established to implement the leakage rate testing of the containment as required by 10 CFR Part 50, Appendix J, Option B, "Performance-Based Requirements.This program shall be in accordance with the guidelines contained in Regulatory Guide 1.163, "Performance-Based Containment Leak-Test Program," dated September 1995. Regulatory Guide 1.163, Section C, "Regulatory Position," further states, in part, that NEI 94-01, Revision 0, dated July 26, 1995, "Industry Guideline for Implementing Performance Based Option of 10 CFR 50, Appendix J" provides methods for complying with the provisions of Option B in Appendix J to 10 CFR Part 50. Contrary to the above, as of June 30, 2013, the licensee failed to implement a program for leakage rate testing of the containment in accordance with Technical Specification 6.5.16. Specifically, Nuclear Energy Institute 94-01, Section 10.2.3.4, states, in part, that if test results are not acceptable, then a cause determination should be performed and corrective actions identified that focus on those activities that can eliminate the identified cause of the failure. A failure, as defined by the standard, is exceeding an administrative limit and not the total failure of the valve. However, the licensee's program for containment leakage rate testing did not require a cause determination and identification of corrective actions to eliminate the cause of the failure. The licensee documented this failure in Condition Report CR-ANO-2-2013-01370. Because this finding is of very low safety significance and has been entered into the corrective action program, this violation is being treated as a non-cited violation consistent with Section 2.3.2.a of the NRC Enforcement Policy:
Unit 2 Technical Specification 6.5.16, Containment Leakage Rate Testing Program, states, in part, that a program shall be established to implement the leakage rate testing of the containment as required by 10 CFR Part 50, Appendix J, Option B, Performance-Based Requirements. This program shall be in accordance with the guidelines contained in Regulatory Guide 1.163, Performance-Based Containment Leak-Test Program, dated September 1995. Regulatory Guide 1.163, Section C, Regulatory Position, further states, in part, that NEI 94-01, Revision 0, dated July 26, 1995, Industry Guideline for Implementing Performance Based Option of 10 CFR 50, Appendix J provides methods for complying with the provisions of Option B in Appendix J to 10 CFR Part 50. Contrary to the above, as of June 30, 2013, the licensee failed to implement a program for leakage rate testing of the containment in accordance with Technical Specification 6.5.16. Specifically, Nuclear Energy Institute 94-01, Section 10.2.3.4, states, in part, that if test results are not acceptable, then a cause determination should be performed and corrective actions identified that focus on those activities that can eliminate the identified cause of the failure. A failure, as defined by the standard, is exceeding an administrative limit and not the total failure of the valve. However, the licensees program for containment leakage rate testing did not require a cause determination and identification of corrective actions to eliminate the cause of the failure. The licensee documented this failure in Condition Report CR-ANO-2-2013-01370. Because this finding is of very low safety significance and has been entered into the corrective action program, this violation is being treated as a non-cited violation consistent with Section 2.3.2.a of the NRC Enforcement Policy:
NCV 05000368/2013003-01, "Failure to Evaluate and Correct Excessive Containment Isolation Valve Leakage."
NCV 05000368/2013003-01, Failure to Evaluate and Correct Excessive Containment Isolation Valve Leakage.


==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection
{{a|4OA1}}
{{a|4OA1}}
==4OA1 Performance Indicator Verification==
==4OA1 Performance Indicator Verification==
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed a review of the performance indicator data submitted by the licensee for the first quarter 2013 performance indicators for any obvious inconsistencies prior to its public release in accordance with Inspection Manual Chapter 0608, "Performance Indicator Program."
The inspectors performed a review of the performance indicator data submitted by the licensee for the first quarter 2013 performance indicators for any obvious inconsistencies prior to its public release in accordance with Inspection Manual Chapter 0608, Performance Indicator Program.


This review was performed as part of the inspectors' normal plant status activities and, as such, did not constitute a separate inspection sample.
This review was performed as part of the inspectors normal plant status activities and, as such, did not constitute a separate inspection sample.


====b. Findings====
====b. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors sampled licensee submittals for the safety system functional failures performance indicator for both Units 1 and 2 for the period from the first quarter 2012 through the first quarter 2013. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6, and NUREG-1022, "Event Reporting Guidelines 10 CFR 50.72 and 50.73." The inspectors reviewed the licensee's operator narrative logs, operability assessments, maintenance rule records, maintenance work orders, issue reports, event reports, and NRC integrated inspection reports for the period of January 2012 through March 2013, to validate the accuracy of the submittals. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report. These activities constitute completion of two safety system functional failures samples as defined in Inspection Procedure 71151-05.
The inspectors sampled licensee submittals for the safety system functional failures performance indicator for both Units 1 and 2 for the period from the first quarter 2012 through the first quarter 2013. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, and NUREG-1022, Event Reporting Guidelines 10 CFR 50.72 and 50.73." The inspectors reviewed the licensees operator narrative logs, operability assessments, maintenance rule records, maintenance work orders, issue reports, event reports, and NRC integrated inspection reports for the period of January 2012 through March 2013, to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report.
 
These activities constitute completion of two safety system functional failures samples as defined in Inspection Procedure 71151-05.


====b. Findings====
====b. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors sampled licensee submittals for the reactor coolant system specific activity performance indicator for both Units 1 and 2 for the period from the second quarter 2012 through the first quarter 2013. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6. The inspectors reviewed the licensee's reactor coolant system chemistry samples, technical specification requirements, issue reports, event reports, and NRC integrated inspection reports for the period of April 2012 through March 2013, to validate the accuracy of the submittals. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. In addition to record reviews, the inspectors observed a chemistry technician obtain and analyze a reactor coolant system sample. Specific documents reviewed are described in the attachment to this report. These activities constitute completion of two reactor coolant system specific activity samples as defined in Inspection Procedure 71151-05.
The inspectors sampled licensee submittals for the reactor coolant system specific activity performance indicator for both Units 1 and 2 for the period from the second quarter 2012 through the first quarter 2013. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6. The inspectors reviewed the licensees reactor coolant system chemistry samples, technical specification requirements, issue reports, event reports, and NRC integrated inspection reports for the period of April 2012 through March 2013, to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. In addition to record reviews, the inspectors observed a chemistry technician obtain and analyze a reactor coolant system sample. Specific documents reviewed are described in the attachment to this report.
 
These activities constitute completion of two reactor coolant system specific activity samples as defined in Inspection Procedure 71151-05.


====b. Findings====
====b. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors sampled licensee submittals for the reactor coolant system leakage performance indicator for both Units 1 and 2 for the period from the second quarter 2012 through the first quarter 2013. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6. The inspectors reviewed the licensee's operator logs, reactor coolant system leakage tracking data, issue reports, event reports, and NRC integrated inspection reports for the period of April 2012 through March 2013 to validate the accuracy of the submittals. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report.
The inspectors sampled licensee submittals for the reactor coolant system leakage performance indicator for both Units 1 and 2 for the period from the second quarter 2012 through the first quarter 2013. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6. The inspectors reviewed the licensees operator logs, reactor coolant system leakage tracking data, issue reports, event reports, and NRC integrated inspection reports for the period of April 2012 through March 2013 to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report.


These activities constitute completion of two reactor coolant system leakage samples as defined in Inspection Procedure 71151-05.
These activities constitute completion of two reactor coolant system leakage samples as defined in Inspection Procedure 71151-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|4OA2}}
{{a|4OA2}}
==4OA2 Problem Identification and Resolution==
==4OA2 Problem Identification and Resolution==
{{IP sample|IP=IP 71152}}
{{IP sample|IP=IP 71152}}
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====a. Inspection Scope====
====a. Inspection Scope====
As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensee's corrective action program at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. The inspectors reviewed attributes that included the complete and accurate identification of the problem; the timely correction, commensurate with the safety significance; the evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and previous occurrences reviews; and the classification, prioritization, focus, and timeliness of corrective actions. Minor issues entered into the licensee's corrective action program because of the inspectors' observations are included in the attached list of documents reviewed.
As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees corrective action program at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. The inspectors reviewed attributes that included the complete and accurate identification of the problem; the timely correction, commensurate with the safety significance; the evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and previous occurrences reviews; and the classification, prioritization, focus, and timeliness of corrective actions. Minor issues entered into the licensees corrective action program because of the inspectors observations are included in the attached list of documents reviewed.


These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure, they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report.
These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure, they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report.
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====a. Inspection Scope====
====a. Inspection Scope====
In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensee's corrective action program. The inspectors accomplished this through review of the station's daily corrective action documents.
In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensees corrective action program. The inspectors accomplished this through review of the stations daily corrective action documents.


The inspectors performed these daily reviews as part of their daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.
The inspectors performed these daily reviews as part of their daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.
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No findings were identified.
No findings were identified.


===.3 Licensee's Actions to Resolve Substantive Cross-Cutting Issue===
===.3 Licensees Actions to Resolve Substantive Cross-Cutting Issue===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed a review of the licensee's corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors focused their review on substantive cross-cutting issue H.1(b), dealing with the licensee's ability to use conservative decision making when evaluating and correcting problems (see Manual Chapter 0310, "Components Within the Cross-Cutting Areas," Dated October 28, 2011, Section 06). The inspectors also discussed performance improvement details with licensee representatives, and performed a review of licensee initiatives to address deficiencies in the conservative decision making process. Documents reviewed by the inspectors are listed in an attachment to this report.
The inspectors performed a review of the licensees corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors focused their review on substantive cross-cutting issue H.1(b), dealing with the licensees ability to use conservative decision making when evaluating and correcting problems (see Manual Chapter 0310, Components Within the Cross-Cutting Areas, Dated October 28, 2011, Section 06). The inspectors also discussed performance improvement details with licensee representatives, and performed a review of licensee initiatives to address deficiencies in the conservative decision making process. Documents reviewed by the inspectors are listed in an attachment to this report.


These activities constitute completion of one in-depth problem identification and resolution sample as defined in Inspection Procedure 71152-05.
These activities constitute completion of one in-depth problem identification and resolution sample as defined in Inspection Procedure 71152-05.


====b. Findings and Observations====
====b. Findings and Observations====
No findings were identified. Overall, the licensee's recovery plan appeared to address the appropriate deficiencies necessary for performance improvement.
No findings were identified. Overall, the licensees recovery plan appeared to address       the appropriate deficiencies necessary for performance improvement.
{{a|4OA3}}
{{a|4OA3}}
==4OA3 Followup of Events and Notices of Enforcement Discretion==
==4OA3 Followup of Events and Notices of Enforcement Discretion==
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(Closed) LER 05000368/2013-002-00, An Inoperable Emergency Control Room Chiller Due to Maintenance Error Results in a Prevented Safety Function.
(Closed) LER 05000368/2013-002-00, An Inoperable Emergency Control Room Chiller Due to Maintenance Error Results in a Prevented Safety Function.


On February 4, 2013, at 1255 CST, control room emergency chiller 2VE-1A breaker tripped shortly after the chiller was started. 2VE-1A is one of the two control room emergency chillers common to both Units 1 and 2. The licensee concluded that the cause of the breaker trip was that the "C" phase load side wire lug was not properly connected when the breaker was installed on November 15, 2012, resulting in a loose connection between the lug and the breaker stab. The condition was corrected and 2VE-1A was declared operable on February 6, 2013. The issue was entered into the corrective action program as Condition Report CR-ANO-2-2013-0233. The licensee's corrective actions, as a result of the incorrectly installed breaker, included performing a human performance error review, including additional procedural requirements for visual verification of lug configuration for future breaker replacements, and reinspecting all previously replaced breakers identified in the extent of condition of the apparent cause evaluation. A Green self-revealing non-cited violation is documented below. This licensee event report is closed.
On February 4, 2013, at 1255 CST, control room emergency chiller 2VE-1A breaker tripped shortly after the chiller was started. 2VE-1A is one of the two control room emergency chillers common to both Units 1 and 2. The licensee concluded that the cause of the breaker trip was that the C phase load side wire lug was not properly connected when the breaker was installed on November 15, 2012, resulting in a loose connection between the lug and the breaker stab. The condition was corrected and 2VE-1A was declared operable on February 6, 2013. The issue was entered into the corrective action program as Condition Report CR-ANO-2-2013-0233. The licensees corrective actions, as a result of the incorrectly installed breaker, included performing a human performance error review, including additional procedural requirements for visual verification of lug configuration for future breaker replacements, and reinspecting all previously replaced breakers identified in the extent of condition of the apparent cause evaluation. A Green self-revealing non-cited violation is documented below. This licensee event report is closed.


Failure to Correctly Install Control Room Emergency Chiller Supply Breaker  
Failure to Correctly Install Control Room Emergency Chiller Supply Breaker


=====Introduction.=====
=====Introduction.=====
Inspectors documented a Green self-revealing non-cited violation of Technical Specification 6.4.1.a for the licensee's failure to implement procedures recommended by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.
Inspectors documented a Green self-revealing non-cited violation of Technical Specification 6.4.1.a for the licensees failure to implement procedures recommended by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.


Specifically, the licensee failed to follow procedures for the replacement of the supply breaker for control room emergency chiller 2VE-1A. As a result, the breaker was installed incorrectly and the chiller was inoperable for over two months.
Specifically, the licensee failed to follow procedures for the replacement of the supply breaker for control room emergency chiller 2VE-1A. As a result, the breaker was installed incorrectly and the chiller was inoperable for over two months.


=====Description.=====
=====Description.=====
On February 4, 2013, the breaker for control room emergency chiller   2VE-1A tripped shortly after the chiller was started. When the electricians removed the molded case circuit breaker for testing they identified that the C phase load side wire lug was not properly installed in the breaker; the lug that tightens the wire down to the breaker stab was installed in front of the breaker stab instead of over it. This resulted in a loose connection between the lug and the breaker stab.
On February 4, 2013, the breaker for control room emergency chiller 2VE-1A tripped shortly after the chiller was started. When the electricians removed the molded case circuit breaker for testing they identified that the C phase load side wire lug was not properly installed in the breaker; the lug that tightens the wire down to the breaker stab was installed in front of the breaker stab instead of over it. This resulted in a loose connection between the lug and the breaker stab.
 
The licensee had installed the breaker in accordance with Procedure 1403.179, Molded Case Circuit Breaker Testing, Revision 20. Step 6.2.3 of Attachment 2 directed personnel to re-terminate the wires on the breaker. The location of this equipment made direct visual observation difficult necessitating the use of equipment, such as mirrors, to confirm proper installation. Although personnel installing the breaker were aware of the potential to incorrectly install the lug, they chose not to perform a visual verification of the connection, believing that if they pulled hard on the wires, and the wires did not pull out, it would confirm the lugs were installed properly. This assumption was incorrect because the wire could still be tightly pinched against the lug with the stab located outside of the lug. The licensee concluded that the causes of the incorrectly installed breaker were inadequate self-checks and peer-checks.


The licensee had installed the breaker in accordance with Procedure 1403.179, "Molded Case Circuit Breaker Testing," Revision 20. Step 6.2.3 of Attachment 2 directed personnel to re-terminate the wires on the breaker. The location of this equipment made direct visual observation difficult necessitating the use of equipment, such as mirrors, to confirm proper installation. Although personnel installing the breaker were aware of the potential to incorrectly install the lug, they chose not to perform a visual verification of the connection, believing that if they pulled hard on the wires, and the wires did not pull out, it would confirm the lugs were installed properly. This assumption was incorrect because the wire could still be tightly pinched against the lug with the stab located outside of the lug. The licensee concluded that the causes of the incorrectly installed breaker were inadequate self-checks and peer-checks.
The breaker, which was installed on November 15, 2012, passed a monthly surveillance test directly after the post maintenance test and then again in December and January.


The breaker, which was installed on November 15, 2012, passed a monthly surveillance test directly after the post maintenance test and then again in December and January. Even though the breaker passed three surveillance tests after its replacement, the licensee submitted a licensee event report because they concluded that the control room emergency chiller had not been operable because it had a loose electrical connection since November.
Even though the breaker passed three surveillance tests after its replacement, the licensee submitted a licensee event report because they concluded that the control room emergency chiller had not been operable because it had a loose electrical connection since November.


The licensee documented the issue in their corrective action program as                     CR-ANO-2-2013-00233. After repairs to the 2VE-1A breaker were made, including verification that the lug was correctly installed, a surveillance test was successfully completed on February 6, 2013. Other subsequent corrective actions included a human performance error review and additional procedural requirements for visual verification of the wire/lug connection for future breaker replacements. In addition, the licensee reinspected all previously replaced breakers identified in the apparent cause evaluation extent of condition.  
The licensee documented the issue in their corrective action program as CR-ANO-2-2013-00233. After repairs to the 2VE-1A breaker were made, including verification that the lug was correctly installed, a surveillance test was successfully completed on February 6, 2013. Other subsequent corrective actions included a human performance error review and additional procedural requirements for visual verification of the wire/lug connection for future breaker replacements. In addition, the licensee reinspected all previously replaced breakers identified in the apparent cause evaluation extent of condition.


=====Analysis.=====
=====Analysis.=====
Inspectors concluded that the failure to follow Procedure 1403.179 for replacement of the A train control room emergency chiller breaker is a performance deficiency. The performance deficiency is more than minor because it was associated with the human performance attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences, and is therefore a finding. Specifically, the loose breaker connection adversely affected the availability and reliability of the control room emergency chiller A.
Inspectors concluded that the failure to follow Procedure 1403.179 for replacement of the A train control room emergency chiller breaker is a performance deficiency. The performance deficiency is more than minor because it was associated
 
with the human performance attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences, and is therefore a finding. Specifically, the loose breaker connection adversely affected the availability and reliability of the control room emergency chiller A.
 
Using Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, and Appendix A, The Significance Determination Process (SDP) for Findings at Power, the inspectors determined that the finding required a detailed risk evaluation because it represented an actual loss of function of at least a single train for longer than its technical specification allowed outage time.
 
The senior reactor analyst performed a detailed risk evaluation using the Arkansas Nuclear One Standardized Plant Analysis Risk models Version 8.19 for Unit 1 and Version 8.21 for Unit 2, and various hand calculations. Additionally, the analyst used the seismic risk quantification method described in the Risk Assessment of Operational Events Handbook, Volume 2, External Events. The following calculations were performed:
* Internal Initiators The analyst noted that the control room emergency chillers are only important to risk if the control room chilled water system is not available. The chilled water system is a fully functional backup to the emergency chillers provided they have electrical power. The chilled water system requires offsite power from either unit to function. Therefore, the dominant risk sequences for the control room emergency chillers will be upon loss of offsite power to both units.
 
The loss of offsite power frequency for either unit at Arkansas Nuclear One is 2.84 x 10-2/year as established in the SPAR model. The analyst used the conditional probabilities provided in Table 9 of the Idaho National Laboratories Loss of Offsite Power, 2011 Update, dated February 2013, to calculate the frequency of both units experiencing a loss of offsite power at the same time.
 
The combined frequency of a loss of offsite power affecting both units at Arkansas Nuclear One was 1.42 x 10-2/year.


Using Manual Chapter 0609, Attachment 4, "Initial Characterization of Findings," and Appendix A, "The Significance Determination Process (SDP) for Findings at Power," the inspectors determined that the finding required a detailed risk evaluation because it represented an actual loss of function of at least a single train for longer than its technical specification allowed outage time. The senior reactor analyst performed a detailed risk evaluation using the Arkansas Nuclear One Standardized Plant Analysis Risk models Version 8.19 for Unit 1 and Version 8.21 for Unit 2, and various hand calculations. Additionally, the analyst used the seismic risk quantification method described in the Risk Assessment of Operational Events Handbook, Volume 2, "External Events."  The following calculations were performed:
The analyst reviewed Engineering Report 95-R-0013-01, Control Room Post Accident Ambient Temperature Requirements to determine the peak temperature limits for control room functionality. The limiting components were the high pressure injection flow instruments in Unit 2 which were designed to survive ambient control room temperatures of 122° F. As a bounding assumption, the analyst assumed that the operators and control room instrumentation could survive a peak of 120° F. From calculation CALC-10-E-0010-05, the analyst noted that Unit 2 heated up more rapidly than Unit 1 upon a postulated loss of cooling with 120° F being reached in 16.6 hours. Using the SPAR model, the analyst calculated a loss of offsite power nonrecovery probability for Unit 2 of
* Internal Initiators  The analyst noted that the control room emergency chillers are only important to risk if the control room chilled water system is not available. The chilled water system is a fully functional backup to the emergency chillers provided they have electrical power. The chilled water system requires offsite power from either unit to function. Therefore, the dominant risk sequences for the control room emergency chillers will be upon loss of offsite power to both units. The loss of offsite power frequency for either unit at Arkansas Nuclear One is 2.84 x 10-2/year as established in the SPAR model. The analyst used the conditional probabilities provided in Table 9 of the Idaho National Laboratories "Loss of Offsite Power," 2011 Update, dated February 2013, to calculate the frequency of both units experiencing a loss of offsite power at the same time.


The combined frequency of a loss of offsite power affecting both units at Arkansas Nuclear One was 1.42 x 10-2/year. The analyst reviewed Engineering Report 95-R-0013-01, "Control Room Post Accident Ambient Temperature Requirements to determine the peak temperature limits for control room functionality. The limiting components were the high pressure injection flow instruments in Unit 2 which were designed to survive ambient control room temperatures of 122° F. As a bounding assumption, the analyst assumed that the operators and control room instrumentation could survive a peak of 120° F. From calculation CALC-10-E-0010-05, the analyst noted that Unit 2 heated up more rapidly than Unit 1 upon a postulated loss of cooling with 120° F being reached in 16.6 hours. Using the SPAR model, the analyst calculated a loss of offsite power nonrecovery probability for Unit 2 of
3.4 x 10-2. This resulted in an unrecovered frequency of losing the control room chilled water system of 4.8 x 10-4/year.


===.4 x 10-2.===
Using the SPAR model, the analyst estimated the failure probability of the control room emergency chillers (2.1 x 10-4) and Chiller 1B (2.4 x 10-2), assuming that Chiller 1A failed from the performance deficiency. Assuming that failure of all cooling for greater than 16.6 hours would require a control room abandonment, the analyst set the conditional core damage probability to 0.1 as assumed in the Electric Power Research Institute, fire-induced vulnerability evaluation method.
This resulted in an unrecovered frequency of losing the control room chilled water system of 4.8 x 10-4/year. Using the SPAR model, the analyst estimated the failure probability of the control room emergency chillers (2.1 x 10-4) and Chiller 1B (2.4 x 10-2), assuming that Chiller 1A failed from the performance deficiency. Assuming that failure of all cooling for greater than 16.6 hours would require a control room abandonment, the analyst set the conditional core damage probability to 0.1 as assumed in the Electric Power Research Institute, fire-induced vulnerability evaluation method.


The baseline conditional core damage frequency (CCDFBase) for this performance deficiency was calculated by multiplying the unrecovered frequency of losing the control room chilled water system (FNR-LOOP) with the failure probability of both trains of emergency chillers (Psys) and the conditional core damage probability of a main control room abandonment (CCDP) as follows:   CCDFBase = FNR-LOOP
The baseline conditional core damage frequency (CCDFBase) for this performance deficiency was calculated by multiplying the unrecovered frequency of losing the control room chilled water system (FNR-LOOP) with the failure probability of both trains of emergency chillers (Psys) and the conditional core damage probability of a main control room abandonment (CCDP) as follows:
CCDFBase       = FNR-LOOP
* Psys
* Psys
* CCDP     = 4.8 x 10-4/year
* CCDP
                        = 4.8 x 10-4/year
* 2.1 x 10-4
* 2.1 x 10-4
* 0.1     = 1.0 x 10-8/year The finding conditional core damage frequency (CCDFCase) was calculated by assuming the failure probability of the chilled water system was now the failure probability of Chiller 1B (Ptrain) as follows:   CCDFCase = FNR-LOOP
* 0.1
                        = 1.0 x 10-8/year The finding conditional core damage frequency (CCDFCase) was calculated by assuming the failure probability of the chilled water system was now the failure probability of Chiller 1B (Ptrain) as follows:
CCDFCase       = FNR-LOOP
* Ptrain
* Ptrain
* CCDP     = 4.8 x 10-4/year
* CCDP
                        = 4.8 x 10-4/year
* 2.4 x 10-2
* 2.4 x 10-2
* 0.1     = 1.2 x 10-6/year The analyst noted that the failure of Chiller 1A resulted from the improper termination of the associated breaker. The analyst assumed that the last time the breaker was successfully cycled resulted in the termination being incapable of providing sufficient current for the next start. The exposure period (EXP) was then determined to be the 25 days from the last successful test on January 10, 2013, until the observed failure on February 4, 2013, plus the 2 days it took to repair the condition and return the chiller to a functional status. Therefore, the incremental conditional core damage probability (ICCDP) for this performance deficiency was calculated as follows:
* 0.1
ICCDP = (CCDFCase - CCDFBase)
                        = 1.2 x 10-6/year The analyst noted that the failure of Chiller 1A resulted from the improper termination of the associated breaker. The analyst assumed that the last time the breaker was successfully cycled resulted in the termination being incapable of providing sufficient current for the next start. The exposure period (EXP) was then determined to be the 25 days from the last successful test on January 10, 2013, until the observed failure on February 4, 2013, plus the 2 days it took to repair the condition and return the chiller to a functional status. Therefore, the incremental conditional core damage probability (ICCDP) for this performance deficiency was calculated as follows:
* EXP / 365     = (1.2 x 10-6/year - 1.0 x 10-8/year)
 
* 27 days / 365 days/year     = 8.4 x 10-8
ICCDP           = (CCDFCase - CCDFBase)
* Seismic Initiator The analyst used the plant-specific SPAR, Version 8.19 for Unit 1 and Version 8.21 for Unit 2 and a seismic model prepared as described in the Risk Assessment of Operational Events Handbook, Volume 2, "External Events," to quantify the risk of this condition. To qualify the affect of the performance deficiency on the seismic risk, the analyst made the following assumptions:
* EXP / 365
o A seismic event that caused the failure of the ceramic insulators in the main switchyard would result in a loss of offsite power o A loss of offsite power caused by a seismic event would not be recoverable over the 24-hour response period assumed in this evaluation o Because differential movement is all that is necessary for failure of the improperly terminated power cable, the analyst assumed that the fragility of the termination was the same as the fragility of the ceramic insulators The analyst used 10 bins to characterize the peak ground acceleration during a postulated seismic event. In accordance with the Handbook rules, the frequency of a seismically induced loss of offsite power was calculated as 8.9 x 10-5/year. In a similar manner, the frequency of a seismically-induced loss of offsite power with the failure of Control Room Emergency Chiller 1A was 3.8 x 10-5/year. Using the method described under internal initiators, the analyst calculated a CCDFBase of 7.8 x 10-9/year and a CCDFCase of 9.0 x 10-7/year. Assuming that Chiller 1A was susceptible to failure during a seismic event for the 83 days from the installation of the breaker on November 15, 2012 until it was restored to a functional state on February 6, 2013, the ICCDP for seismic events was calculated to be 2.0 x 10-7. In accordance with NRC Inspection Manual Chapter 0609, Appendix H, Table 5.1, "Phase 1 Screening - Type A Findings at Full Power," none of the core damage sequences affected by this performance deficiency were important to the large, early release frequency. Therefore, based on the combined internal and seismic ICCDP of 2.9 x 10-7, this finding was of very low safety significance (Green).
                                  = (1.2 x 10-6/year - 1.0 x 10-8/year)
* 27 days / 365 days/year
                                  = 8.4 x 10-8
* Seismic Initiator The analyst used the plant-specific SPAR, Version 8.19 for Unit 1 and Version 8.21 for Unit 2 and a seismic model prepared as described in the Risk Assessment of Operational Events Handbook, Volume 2, External Events, to quantify the risk of this condition. To qualify the affect of the performance deficiency on the seismic risk, the analyst made the following assumptions:
o   A seismic event that caused the failure of the ceramic insulators in the main switchyard would result in a loss of offsite power o   A loss of offsite power caused by a seismic event would not be recoverable over the 24-hour response period assumed in this evaluation o   Because differential movement is all that is necessary for failure of the improperly terminated power cable, the analyst assumed that the fragility of the termination was the same as the fragility of the ceramic insulators The analyst used 10 bins to characterize the peak ground acceleration during a postulated seismic event. In accordance with the Handbook rules, the frequency of a seismically induced loss of offsite power was calculated as 8.9 x 10-5/year.
 
In a similar manner, the frequency of a seismically-induced loss of offsite power with the failure of Control Room Emergency Chiller 1A was 3.8 x 10-5/year.
 
Using the method described under internal initiators, the analyst calculated a CCDFBase of 7.8 x 10-9/year and a CCDFCase of 9.0 x 10-7/year. Assuming that Chiller 1A was susceptible to failure during a seismic event for the 83 days from the installation of the breaker on November 15, 2012 until it was restored to a functional state on February 6, 2013, the ICCDP for seismic events was calculated to be 2.0 x 10-7.
 
In accordance with NRC Inspection Manual Chapter 0609, Appendix H, Table 5.1, Phase 1 Screening - Type A Findings at Full Power, none of the core damage sequences affected by this performance deficiency were important to the large, early release frequency. Therefore, based on the combined internal and seismic ICCDP of 2.9 x 10-7, this finding was of very low safety significance (Green).
 
The finding was determined to have a cross-cutting aspect in the area of human performance, associated with work practices, in that the licensee failed to use work practices that support human performance. Specifically, licensee personnel were aware


The finding was determined to have a cross-cutting aspect in the area of human performance, associated with work practices, in that the licensee failed to use work practices that support human performance. Specifically, licensee personnel were aware of the possibility of misaligning the wire grip style lug, but failed to use adequate self and peer checking to ensure the lug was correctly installed [H.4(a)].  
of the possibility of misaligning the wire grip style lug, but failed to use adequate self and peer checking to ensure the lug was correctly installed [H.4(a)].


=====Enforcement.=====
=====Enforcement.=====
Technical Specification 6.4.1.a requires, in part, that written procedures be implemented covering the activities in Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978. Regulatory Guide 1.33, Appendix A, Section 9, specifies that procedures for performing maintenance that can affect the performance of safety-related equipment should be properly pre-planned and completed in accordance with written procedures and documented instructions appropriate to the circumstances.
Technical Specification 6.4.1.a requires, in part, that written procedures be implemented covering the activities in Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978. Regulatory Guide 1.33, Appendix A, Section 9, specifies that procedures for performing maintenance that can affect the performance of safety-related equipment should be properly pre-planned and completed in accordance with written procedures and documented instructions appropriate to the circumstances.


Licensee Procedure 1403.179, "Molded Case Circuit Breaker Testing," Revision 20, was a written procedure that implemented maintenance activities that can affect the performance of safety-related equipment. Procedure 1403.179, Attachment 2, Step 6.2.3 stated, in part, to re-terminate the wires on the breaker. Contrary to the above, the licensee failed to implement procedures covering maintenance activities that could affect the performance of safety-related equipment. Specifically, on November 15, 2012, the licensee failed to follow Procedure 1403.179 and properly re-terminate the wires on the train A control room emergency chiller supply breaker. After repairs to the 2VE-1A breaker were made, including verification that the lug was correctly installed, a surveillance test was successfully completed on February 6, 2013. Because this finding is of very low safety significance and has been entered into the corrective action program as Condition Report CR-ANO-2-2013-00233, this violation is being treated as a non-cited violation consistent with Section 2.3.2.a of the NRC Enforcement Policy:
Licensee Procedure 1403.179, Molded Case Circuit Breaker Testing, Revision 20, was a written procedure that implemented maintenance activities that can affect the performance of safety-related equipment. Procedure 1403.179, Attachment 2, Step 6.2.3 stated, in part, to re-terminate the wires on the breaker. Contrary to the above, the licensee failed to implement procedures covering maintenance activities that could affect the performance of safety-related equipment. Specifically, on November 15, 2012, the licensee failed to follow Procedure 1403.179 and properly re-terminate the wires on the train A control room emergency chiller supply breaker. After repairs to the 2VE-1A breaker were made, including verification that the lug was correctly installed, a surveillance test was successfully completed on February 6, 2013. Because this finding is of very low safety significance and has been entered into the corrective action program as Condition Report CR-ANO-2-2013-00233, this violation is being treated as a non-cited violation consistent with Section 2.3.2.a of the NRC Enforcement Policy:
NCV 05000368/2013003-02, "Failure to Correctly Install Control Room Emergency Chiller Supply Breaker."
NCV 05000368/2013003-02, Failure to Correctly Install Control Room Emergency Chiller Supply Breaker.
 
{{a|4OA5}}
{{a|4OA5}}
==4OA5 Other Activities==
==4OA5 Other Activities==


===.1 (Discussed) NRC Temporary Instruction 2515/182, "Review of the Implementation of the Industry Initiative to Control Degradation of Underground Piping and Tanks"===
===.1 (Discussed) NRC Temporary Instruction 2515/182, Review of the Implementation of the===
Leakage from buried and underground pipes has resulted in ground water contamination incidents with associated heightened NRC and public interest. The industry issued a guidance document, Nuclear Energy Institute 09-14, "Guideline for the Management of Buried Piping Integrity" (ADAMS Accession No. ML1030901420) to describe the goals and commitments made by the licensee resulting from this underground piping and tank initiative. On December 31, 2010, the Nuclear Energy Institute issued Revision 1 to Nuclear Energy Institute 09-14 (ADAMS Accession No. ML110700122) with an expanded scope of components which included underground piping that was not in direct contact with the soil and underground tanks. On November 17, 2011, the NRC issued Temporary Instruction 2515/182, "Review of the Industry Initiative to Control Degradation of Underground Piping and Tanks," to gather information related to the industry's implementation of this initiative.
 
Industry Initiative to Control Degradation of Underground Piping and Tanks Leakage from buried and underground pipes has resulted in ground water contamination incidents with associated heightened NRC and public interest. The industry issued a guidance document, Nuclear Energy Institute 09-14, Guideline for the Management of Buried Piping Integrity (ADAMS Accession No. ML1030901420) to describe the goals and commitments made by the licensee resulting from this underground piping and tank initiative. On December 31, 2010, the Nuclear Energy Institute issued Revision 1 to Nuclear Energy Institute 09-14 (ADAMS Accession No. ML110700122) with an expanded scope of components which included underground piping that was not in direct contact with the soil and underground tanks. On November 17, 2011, the NRC issued Temporary Instruction 2515/182, Review of the Industry Initiative to Control Degradation of Underground Piping and Tanks, to gather information related to the industrys implementation of this initiative.


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the licensee's programs for buried pipe, underground piping, and tanks in accordance with Temporary Instruction 2515/182 to determine if the program attributes and completion dates identified in Sections 3.3 A and 3.3 B of Nuclear Energy Institute 09-14, Revision 1, were contained in the licensee's program and implementing procedures. For the buried pipe and underground piping program attributes with completion dates that had passed, the inspectors reviewed records to determine if the attribute was in fact complete.
The inspectors reviewed the licensees programs for buried pipe, underground piping, and tanks in accordance with Temporary Instruction 2515/182 to determine if the program attributes and completion dates identified in Sections 3.3 A and 3.3 B of
 
Nuclear Energy Institute 09-14, Revision 1, were contained in the licensees program and implementing procedures. For the buried pipe and underground piping program attributes with completion dates that had passed, the inspectors reviewed records to determine if the attribute was in fact complete.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


===.2 (Closed) Temporary Instruction 2515/187, Inspection of Near-Term Task Force Recommendation 2.3 Flooding Walkdowns===
===.2 (Closed) Temporary Instruction 2515/187, Inspection of Near-Term Task Force===
 
Recommendation 2.3 Flooding Walkdowns


====a. Inspection Scope====
====a. Inspection Scope====
Inspectors verified that licensee's walkdown packages for the Units 1 and 2 intake structures contained the elements as specified in Nuclear Energy Institute 12-07 Walkdown Guidance. The inspectors independently performed a walkdown of the Units 1 and 2 intake structures. The inspectors confirmed that the licensee verified the following flood protection features:
Inspectors verified that licensees walkdown packages for the Units 1 and 2 intake structures contained the elements as specified in Nuclear Energy Institute 12-07 Walkdown Guidance.
 
The inspectors independently performed a walkdown of the Units 1 and 2 intake structures. The inspectors confirmed that the licensee verified the following flood protection features:
* External visual inspection for indications of degradation that would prevent its credited function from being performed was performed
* External visual inspection for indications of degradation that would prevent its credited function from being performed was performed
* Critical structure, system, and component dimensions were measured
* Critical structure, system, and component dimensions were measured
* Available physical margin, where applicable, was determined
* Available physical margin, where applicable, was determined
* Flood protection feature functionality was determined using either visual observation or by review of other documents The inspectors verified that non-compliances with current licensing requirements, and issues identified in accordance with the 10 CFR 50.54(f) letter, Item 2.g of Enclosure 4, were entered into the licensee's corrective action program. In addition, issues identified in response to Item 2.g that could challenge risk significant equipment and the licensee's ability to mitigate the consequences will be subject to additional NRC evaluation.
* Flood protection feature functionality was determined using either visual observation or by review of other documents The inspectors verified that non-compliances with current licensing requirements, and issues identified in accordance with the 10 CFR 50.54(f) letter, Item 2.g of Enclosure 4, were entered into the licensee's corrective action program. In addition, issues identified in response to Item 2.g that could challenge risk significant equipment and the licensees ability to mitigate the consequences will be subject to additional NRC evaluation.


====b. Findings====
====b. Findings====
No findings identified.
No findings identified.


===.3 (Closed) Temporary Instruction 2515/188, Inspection of Near-Term Task Force Recommendation 2.3 Seismic Walkdowns===
===.3 (Closed) Temporary Instruction 2515/188, Inspection of Near-Term Task Force===
 
Recommendation 2.3 Seismic Walkdowns


====a. Inspection Scope====
====a. Inspection Scope====
Line 560: Line 649:
* The area appeared to be free of potentially adverse seismic interactions that could cause flooding or spray in the area
* The area appeared to be free of potentially adverse seismic interactions that could cause flooding or spray in the area
* The area appeared to be free of potentially adverse seismic interactions that could cause a fire in the area
* The area appeared to be free of potentially adverse seismic interactions that could cause a fire in the area
* The area appeared to be free of potentially adverse seismic interactions associated with housekeeping practices, storage of portable equipment, and temporary installations (e.g., scaffolding, lead shielding) Observations made during the walkdown that could not be determined to be acceptable were entered into the licensee's corrective action program for evaluation.
* The area appeared to be free of potentially adverse seismic interactions associated with housekeeping practices, storage of portable equipment, and temporary installations (e.g., scaffolding, lead shielding)
Observations made during the walkdown that could not be determined to be acceptable were entered into the licensees corrective action program for evaluation.


====b. Findings====
====b. Findings====
No findings identified.
No findings identified.


{{a|OA6}}
{{a|4OA6}}
==OA6 Meetings, Including Exit Exit Meeting Summary On May 16, 2013, the inspectors presented the inspection results of the review of inservice inspection activities to Mr. D. James, Nuclear Safety Assurance Director, and other members of==
==4OA6 Meetings, Including Exit==


the licensee staff. The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.
===Exit Meeting Summary===
 
On May 16, 2013, the inspectors presented the inspection results of the review of inservice inspection activities to Mr. D. James, Nuclear Safety Assurance Director, and other members of the licensee staff. The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.


On July 2, 2013, the inspectors presented the inspection results to Mr. J. Browning, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.
On July 2, 2013, the inspectors presented the inspection results to Mr. J. Browning, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.
A1-


=SUPPLEMENTAL INFORMATION=
=SUPPLEMENTAL INFORMATION=
Line 579: Line 669:


===Licensee Personnel===
===Licensee Personnel===
: [[contact::A. Remer]], Project Manager  
: [[contact::A. Remer]], Project Manager
: [[contact::B. Greeson]], Engineering, Procurement Manager  
: [[contact::B. Greeson]], Engineering, Procurement Manager
: [[contact::D. Hughes]], Engineering Supervisor  
: [[contact::D. Hughes]], Engineering Supervisor
: [[contact::D. James]], Nuclear Safety Assurance Director  
: [[contact::D. James]], Nuclear Safety Assurance Director
: [[contact::D. Meatheany]], Steam Generator Lead  
: [[contact::D. Meatheany]], Steam Generator Lead
: [[contact::D. Perkins]], Maintenance Manager  
: [[contact::D. Perkins]], Maintenance Manager
: [[contact::J. Browning]], Site Vice President  
: [[contact::J. Browning]], Site Vice President
: [[contact::J. Gobell]], Welding Engineer  
: [[contact::J. Gobell]], Welding Engineer
: [[contact::J. Tobin]], Security Manager  
: [[contact::J. Tobin]], Security Manager
: [[contact::K. Panther]], Nondestructive Examination Lead  
: [[contact::K. Panther]], Nondestructive Examination Lead
: [[contact::M. Chisum]], General Manager Plant Operations  
: [[contact::M. Chisum]], General Manager Plant Operations
: [[contact::M. Hall]], Licensing Specialist  
: [[contact::M. Hall]], Licensing Specialist
: [[contact::N. Mosher]], Licensing Specialist  
: [[contact::N. Mosher]], Licensing Specialist
: [[contact::P. Schlutermor]], Boric Acid Lead  
: [[contact::P. Schlutermor]], Boric Acid Lead
: [[contact::R. Fuller]], Nuclear Oversight Manager  
: [[contact::R. Fuller]], Nuclear Oversight Manager
: [[contact::S. Pyle]], Licensing Manager  
: [[contact::S. Pyle]], Licensing Manager


==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==


===Opened and Closed===
===Opened and Closed===
: 05000368/2013003-01 NCV Failure to Evaluate and Correct Excessive Containment Isolation Valve Leakage (Section 1R22)  
: 05000368/2013003-01 NCV Failure to Evaluate and Correct Excessive Containment Isolation Valve Leakage (Section 1R22)
: 05000368/2013003-02 NCV Failure to Correctly Install Control Room Emergency Chiller Supply Breaker (Section 40A3)
: 05000368/2013003-02 NCV Failure to Correctly Install Control Room Emergency Chiller Supply Breaker (Section 40A3)
 
===Closed===
===Closed===
: [[Closes LER::05000368/LER-2013-002]]-00 LER An Inoperable Emergency Control Room Chiller Due to Maintenance Error Results in a Prevented Safety Function
(Section 4OA3) 2515/187 TI Inspection of Near-Term Task Force Recommendation 2.3 Flooding Walkdowns (Section 4OA5.2) 
: Attachment 1 2515/188 TI Inspection of Near-Term Task Force Recommendation 2.3 Seismic Walkdowns (Section 4OA5.3)  Discussed 2515/182 TI Review of the Implementation of the Industry Initiative to Control Degredation of Underground Piping and Tanks (Section 4OA5.1) 
==LIST OF DOCUMENTS REVIEWED==
==Section 1R01: Adverse Weather ProtectionPROCEDURES==
: NUMBER TITLE REVISION
: OP-1203.025 Natural Emergencies 040
: ENS-DC-199 Off Site Power Supply Design Requirements Nuclear Plant Interface Requirements 8
: OP-1203.037 Abnormal ES Bus Votage and Degraded Offsite Power 010
: OP-1202.007 Degraded Power 012
: 5310.002 Offsite Power System Voltage Reevaluation 002
: ENS-DC-201 ENS Transmission Grid Monitoring 6


==Section 1R04: Equipment AlignmentPROCEDURES==
An Inoperable Emergency Control Room Chiller Due to
: NUMBER TITLE REVISION
: 05000368/2013-002-00 LER        Maintenance Error Results in a Prevented Safety Function (Section 4OA3)
: OP-1104.036 Emergency Diesel Generator Operation 065
Inspection of Near-Term Task Force Recommendation 2.3 2515/187                  TI Flooding Walkdowns (Section 4OA5.2)
: OP-2104.039 HPSI System Operation 073
Attachment 1
: OP-1015.016 Unit Two Operations Forms 036
: OP-1015.001 Conduct of Operations 096
: OP-2106.006 Emergency Feedwater System Operations 083 
: CALCULATION NUMBER TITLE REVISION
: 91-E-0016-154 Piping Qualification of line 2DCB-2-4 from anchor 2DCB-2-H5 to capped free end 040   
: Attachment 1 CONDITION REPORT
: CR-ANO-2-2013-01194


==Section 1R05: Fire Protection==
Inspection of Near-Term Task Force Recommendation 2.3 2515/188                TI Seismic Walkdowns (Section 4OA5.3)
: PROCEDURES NUMBER TITLE REVISION
: PFP-U1 ANO Pre-Fire Plan Unit 1 15
: PFP-U2 ANO Pre-Fire Plan Unit 2 11


==Section 1R06: Flood Protection Measures==
===Discussed===
: PROCEDURES NUMBER TITLE REVISION
: OP-1104.029 Service Water and Auxiliary Cooling System 99
: OP-2104.029 Service Water System Operations 93
: CONDITION REPORTS
: CR-ANO-1-2003-0584
: CR-ANO-2-2006-0367CR-ANO-1-2011-0495CR-ANO-C-2012-0616
: CR-ANO-1-2012-1571
: CR-ANO-1-2012-1627CR-ANO-2-2012-2967
: MISCELLANEOUS NUMBER TITLE REVISION
: ER 963202E101 Intake Structure Roof Missile Shield Rain Guard Installation 0


==Section 1R08: Inservice Inspection Activities==
Review of the Implementation of the Industry Initiative to Control 2515/182              TI Degredation of Underground Piping and Tanks (Section 4OA5.1)
: PROCEDURES 
: NUMBER TITLE REVISION
: CEP-NDE-0404 Manual Ultrasonic Examination of Ferritic Piping Welds (ASME XI)
: CEP-NDE-0255 Radiographic Examination ASME, ANSI, AWS, Welds, and Components
: 6
: CEP-NDE-0400 Ultrasonic Examination 3 
: Attachment 1


==Section 1R08: Inservice Inspection Activities==
==LIST OF DOCUMENTS REVIEWED==
: PROCEDURES
: NUMBER TITLE REVISION
: CEP-NDE-0731 Magnetic Particle Examination (MT) for ASME Section XI
: 3
: CEP-NDE-0504 Ultrasonic Examination of Small Bore Diameter Piping for Thermal Fatigue Damage
: CEP-NDE-0485 Manual Ultrasonic Examination of Vessel Nozzle Inside Radius (Non-App VIII) 9
: SEP-BAC-ANO-001 Boric Acid Corrosion Control Program Inspection And Identification Of Boric Acid Leaks For
: ANO-1 And
: ANO-2
: CEP-BAC-001 Boric Acid Corrosion Control (BACC) Program Plan 0
: EN-DC-319 Inspection and Evaluation of Boric Acid Leaks 8 
: MISCELLANEOUS 
: NUMBER TITLE DATE
: ANO-1 Steam Generator Tube Inspection Discussion Points May 10, 2013 CONDITION REPORTS
: CR-ANO-1-2012-00137
: CR-ANO-1-2012-00142
: CR-ANO-1-2012-00155
: CR-ANO-1-2012-01470
: CR-ANO-1-2012-01391
: CR-ANO-1-2013-00635
: CR-ANO-1-2012-00831
: CR-ANO-1-2012-01358
: CR-ANO-1-2012-01362
: CR-ANO-1-2012-01363
: CR-ANO-1-2012-01387
: CR-ANO-1-2012-01610
: CR-ANO-1-2013-00479
: WORK ORDERS
: 338728-03
: 338729-03     
: Attachment 1
 
==Section 1R11: Licensed Operator Requalification Program==
: MISCELLANEOUS 
: NUMBER TITLE REVISION
: A1JPM-RO-AOP32 Perform Spent Fuel Pool Makeup 1 A1JPM-RO-AOP15 Followup Actions for Remote Shutdown, without Auxiliary Feedwater Pump 5 A2JPM-RO-2RS2A Perform Startup of 2Y2224 (Swing Inverter for 2RS2) (Alternate Success Path) 5 A2JPM-RO-LOF01 Align Condensate Pump for Start During a Loss of All Feedwater Event 4
: PROCEDURE 
: NUMBER TITLE REVISION
: OP-1105.009 CRD System Operating Procedure 42
 
==Section 1R12: Maintenance Effectiveness==
: WORK ORDER
: 00286870-01
 
==Section 1R13: Maintenance Risk Assessment and Emergent Work Controls==
: PROCEDURES NUMBER TITLE REVISION
: COPD-024 Risk Assessment Guidelines 45
: COPD-024 Risk Assessment Guidelines 46
: OP-1015.033 ANO Switchyard and Transformer Yard Controls 20
: OP-1015.033 ANO Switchyard and Transformer Yard Controls 23
: OP-1203.025 Natural Emergencies 35 
: Attachment 1
 
==Section 1R13: Maintenance Risk Assessment and Emergent Work Controls==
: PROCEDURES NUMBER TITLE REVISION
: COPD-024 Risk Assessment Guidelines 45
: EN-WM-104
: EN-OP-119 On Line Risk Assessment Protected Equipment Postings 7
: 5
: OP-1015.048 Shutdown Operations Protection Plan 005
: EN-OU-108 Shutdown Safety Management Program (SSMP) 5
: OP-2203.008 Natural Emergencies 24
: EN-OP-111 Operational Decision-Making Issue (ODMI) Process 10
: EN-OP-116 Infrequently Performed Tests or Evolutions 11
: CONDITION REPORTS
: CR-ANO-C-2013-0063
: CR-ANO-2-2013-1029
: MISCELLANEOUS NUMBER TITLE REVISION
: 1R24 Outage Risk Assessment Team Report 2
: Job Hazard Analysis for Removal of Stator and Goldhofer from the Train Bay
 
==Section 1R15: Operability Evaluations==
: PROCEDURES NUMBER TITLE REVISION
: EN-OP-104 Operability Evaluations 5
: OP-1203.025 Natural Emergencies (Unit 1) 40
: OP-2203.008 Natural Emergencies (Unit 2) 25
: CONDITION REPORTS
: CR-ANO-C-2012-03071
: CR-ANO-C-2012-03371
: CR-ANO-1-2013-00183
: CR-ANO-C-2013-00787
: CR-ANO-2-2013-00855
: CR-ANO-2-2013-01029 
: Attachment 1
: CR-ANO-2-2013-01205
: CR-ANO-1-2013-01458
: CR-ANO-1-2011-02277 ENGINEERING CHANGES
: 33072 35761 
: WORK ORDERS
: 52398755-01
: 52326271-01
: 52397520-01 
: MISCELLANEOUS NUMBER TITLE REVISION
: TDQ011 0050 Instructions for Qualitrol Pressure Indicator Relay 509-100,
: IED 509 series, 900 series, 910 series 0
: ULD-0-TOP-17 ANO Flooding Topical 0 
: DRAWINGS NUMBER TITLE REVISION
: EBB-6-H13 Hanger Detail Steam Generator 1
: MS-228 Small Pipe Isometric Steam Generator E-24B Upper Tube Sheet South Vent 3
: CALCULATIONS NUMBER TITLE REVISION
: 92-E-0077-08 Maximum LPI Flow from the RB Sump 0 80D-1103-02 OTSG Upper Tube Sheet Vent South 3
 
==Section 1R18: Plant Modifications==
: PROCEDURES NUMBER TITLE REVISION
: OP-1304.057 Unit 1 Source Range Channels Calibration 20
: EN-OP-111 Operational Decision-Making Issue (ODMI) Process 10
: OP-1015.037 Post Transient Review 17 
: Attachment 1 WORK ORDERS
: 00348095
: 03448996
: ENGINEERING CHANGES
: 43758 43686
: CONDITION REPORTS
: CR-ANO-1-2012-01134
: CR-ANO-1-2012-01683
: CR-ANO-1-2012-01852
: CR-ANO-1-2013-00217
: CR-ANO-1-2013-00551
: CR-ANO-1-2013-01010
: CR-ANO-1-2013-01012
: MISCELLANEOUS NUMBER TITLE REVISION  / DATE
: EC 5512 Temporary Modification Evaluation Memo, ANO Unit 1 Gamma-Metrics Source Range Channel Operability Guidance Oct 11, 2002
: STM-67 Systems Training Manual - Nuclear Instrumentation 11
 
==Section 1R19: Post-Maintenance Testing==
: PROCEDURE NUMBER TITLE REVISION
: OP-1412.001 Preventitive Maintenance of Limitorque SB/SMB Motor Operators 37
: WORK ORDERS
: 52403146-01 52366911-01
 
==Section 1R20: Refueling and Other Outage Activities==
: PROCEDURES NUMBER TITLE REVISION
: OP-1504.007 Unit 1 Reactor Vessel Closure Head Removal and Storage 024 
: Attachment 1
 
==Section 1R20: Refueling and Other Outage Activities==
: PROCEDURES NUMBER TITLE REVISION
: OP-1104.004 Decay Heat Removal Operating Procedure 106
: OP-1204.043 Refueling Abnormal Operation 8
: OP-1502.010 Control of Fuel and Control Rod Movement in Unit 1 Spent Fuel Area 19
: OP-1502.003 Refueling Equipment and Operator Checkouts 40
: OP-1502.004 Control of Unit 1 Refueling 52
: OP-1506.001 Fuel and Control Component Handling 46
 
==Section 1R22: Surveillance Testing==
: PROCEDURES NUMBER TITLE REVISION
: OP-2305.017 Local Leak Rate Testing 29
: EN-DC-334 Primary Containment Leak Rate Testing (Appendix J) 1
: SEP-APJ-002 ANO Primary Containment Leakage Rate Testing (Appendix J) Program Section 0
: OP-2104.037 Alternate ac Diesel Generator Operations 24
: OP-1104.036 Emergency Diesel Generator Operation 062
: OP-2305.016 Remote Features Periodic Testing 025
: OP-2104.036 Emergency Diesel Generator Operations 084
: OP-2106.006 Emergency Feedwater System Operations 083
: CONDITION REPORTS
: CR-ANO-2-2005-1062
: CR-ANO-2-2008-0678CR-ANO-22-11-0800
: CR-ANO-2-2011-1194
: CR-ANO-2-2012-1789
: CR-ANO-2-2012-2270CR-ANO-2-2012-2846CR-ANO-C-2013-0310
: CR-ANO-C-2013-0331CR-ANO-C-2013-332
: CR-ANO-C-2013-353
: CR-ANO-C-2013-0384
: MISCELLANEOUS NUMBER TITLE REVISION
: NEI-94-01 Industry Guidline for Implementing Performance-Based 2-A 
: Attachment 1 MISCELLANEOUS NUMBER TITLE REVISION
: Option of 10CFR Part 50, Appendix J CALCULATIONS NUMBER TITLE REVISION
: CALC-82-D-2086-01 Volume of CST T-41B Requiring Tornado Missile Protection 2-A 01-E-0044-01 QCST Level for Required Tech Spec Volume 0 99-E-0013-01 Adequacy of QCST (T41-B) to Supply Steam Generator Inventory for
: PSA 24-Hour Mission Time 0
 
==Section 4OA1: Performance Indicator Verification==
: PROCEDURES NUMBER TITLE REVISION
: EN-FAP-EP-005 Fleet Administrative Procedure - Emergency Preparedness Indicators 0
: EN-LI-114 Performance Indicator Process 6
 
==Section 4OA2: Identification and Resolution of Problems==
: CONDITION REPORTS
: CR-ANO-1-2013-00599
: CR-ANO-1-2011-02277
: CR-ANO-1-2013-01217
: CR-ANO-2-2013-00963
: CR-ANO-1-2013-01199
: CR-ANO-1-2012-00255
: CR-ANO-1-2013-01634
: CR-ANO-1-2013-01569
: CR-ANO-C-2013-00736
: PROCEDURE NUMBER TITLE REVISION
: OP-1305.038 Unit 1 Local Leak Rate Testing of Electrical Penetrations 000
: WORK ORDER
: 50233933-01   
: Attachment 1


==Section 4OA5: Other Activities==
: PROCEDURES NUMBER TITLE REVISION
: 1203.025 Natural Emergencies 40 2203.008 Natural Emergencies 26
: CEP-UPT-0100 Underground Piping and Tanks Inspection and Monitoring 2 
: MISCELLANEOUS DOCUMENTS NUMBER TITLE REVISION
: EC-40635 Fukushima NTTF Rec. 2.3 Seismic and Flooding Walkdown Reports 0 ENTGCORP13-RPT-002 Att. C Flooding Walkdown Package WP26
: Buried Pipe and Tank Inspection and Monitoring Program, Long Range Plan
: 3 
: Attachment 2
: SUBJECT: Arkansas Nuclear One Unit 1 - Notification Of Inspection (NRC Inspection Report And Request For Information) From April 1 to April 12, 2013, reactor inspectors from the Nuclear Regulatory Commission's (NRC) Region IV office will perform the baseline inservice inspection at Arkansas Nuclear One Unit 1, using NRC Inspection Procedure 71111.08, "Inservice Inspection Activities."
: Experience has shown that this inspection is a resource intensive inspection both for the NRC inspectors and your staff.
: In order to minimize the impact to your onsite resources and to ensure a productive inspection, we have enclosed a request for documents needed for this inspection.
: These documents have been divided into two groups.
: The first group (Section A of the enclosure), due by February 19, 2013, identifies information to be provided prior to the inspection to ensure that the inspectors are adequately prepared.
: The second group (Section B
of the enclosure) identifies the information the inspectors will need upon arrival at the site.
: It is important that all of these documents are up to date and complete in order to minimize the number of additional documents requested during the preparation and/or the onsite portions of the inspection. We have discussed the schedule for these inspection activities with your staff and understand that our regulatory contact for this inspection will be Ms. Natalie Mosher of your licensing organization.
: Our inspection dates are subject to change based on your updated schedule of outage activities.
: If there are any questions about this inspection or the material requested, please contact Jim Drake at (817) 200-1558 (James.Drake@nrc.gov). This letter does not contain new or amended information collection requirements subject to the Paperwork Reduction Act of 1995 (44 U.S.C. 3501 et seq.).
: Existing information collection requirements were approved by the Office of Management and Budget, Control Number 3150-0011.
: The NRC may not conduct or sponsor, and a person is not required to respond to, a request for information or an information collection requirement unless the requesting document displays a currently valid Office of Management and Budget control number. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS).
: ADAMS is accessible from the NRC web site at    http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room) 
: Attachment 2 INSERVICE INSPECTION DOCUMENT REQUEST Inspection Dates: April 1 through April 12, 2013 
: Inspection Procedures:
: IP 71111.08 "Inservice Inspection (ISI) Activities" Inspectors: Jim Drake, Senior Reactor Inspector (Lead Inspector - ISI) A. Information Requested for the In-Office Preparation Week The following information should be sent to the Region IV office in hard copy or electronic format (ims.certrec.com preferred), in care of Jim Drake, by March 11, 2013, to facilitate the selection of specific items that will be reviewed during the onsite inspection week.
: The inspectors will select specific items from the information requested below and then request from your staff additional documents needed during the onsite inspection week (Section B of this enclosure).
: We ask that the specific items selected from the lists be available and ready for review on the first day of inspection.
: Please provide requested documentation electronically if possible.
: If requested documents are large and only hard copy formats are available, please inform the inspector(s), and provide subject documentation during the first day of the onsite inspection.
: If you have any questions regarding this information request, please call the inspector as soon as possible. A.1 ISI/Welding Programs and Schedule Information a) A detailed schedule (including preliminary dates) of: i)
: Nondestructive examinations planned for Class 1 and 2 systems and containment, performed as part of your ASME Section XI, risk informed (if applicable), and augmented inservice inspection programs during the upcoming outage. Provide a status summary of the nondestructive examination inspection activities vs. the required inspection period percentages for this interval by category per ASME Section XI,
: IWX-2400.
: Do not provide separately if other documentation requested contains this information. ii)
: Reactor pressure vessel head examinations planned for the upcoming outage. iii) Examinations planned for Alloy 82/182/600 components that are not included in the Section XI scope (If applicable). iv) Examinations planned as part of your boric acid corrosion control program (Mode 3 walkdowns, bolted connection walkdowns, etc.). v) Welding activities that are scheduled to be completed during the upcoming outage (ASME Class 1, 2, or 3 structures, systems, or components). 
: Attachment 2  b) A copy of ASME Section XI Code Relief Requests and associated NRC safety evaluations applicable to the examinations identified above. c) A list of nondestructive examination reports (ultrasonic, radiography, magnetic particle, dye penetrant, Visual
: VT-1,
: VT-2, and
: VT-3), which have identified relevant conditions on Code Class 1 and 2 systems since the beginning of the last refueling outage.
: This should include the previous Section XI pressure test(s) conducted during start up and any evaluations associated with the results of the pressure tests.
: Also, include in the list the nondestructive examination reports with relevant conditions in the reactor pressure vessel head penetration nozzles that have been accepted for continued service.
: The list of nondestructive examination reports should include a brief description of the structures, systems, or components where the relevant condition was identified. d) A list with a brief description (e.g., system, material, pipe size, weld number, and nondestructive examinations performed) of the welds in Code Class 1 and 2 systems which have been fabricated due to component repair/replacement activities since the beginning of the last refueling outage, or are planned to be fabricated this refueling outage. e) If reactor vessel weld examinations required by the ASME Code are scheduled to occur during the upcoming outage, provide a detailed description of the welds to be examined and the extent of the planned examination.
: Please also provide reference numbers for applicable procedures that will be used to conduct these examinations. f) Copy of any 10 CFR Part 21 reports applicable to your structures, systems, or components within the scope of Section XI of the ASME Code that have been identified since the beginning of the last refueling outage. g)
: A list of any temporary noncode repairs in service (e.g., pinhole leaks). h) Please provide copies of the most recent self-assessments for the inservice inspection, welding, and Alloy 600 programs.
: A.2 Reactor Pressure Vessel Head  a)
: Provide the detailed scope of the planned nondestructive examinations of the reactor vessel head which identifies the types of nondestructive examination methods to be used on each specific part of the vessel head to fulfill commitments made in response to NRC Bulletin 2002-02 and
: NRC Order
: EA-03-009.
: Also, include examination scope expansion criteria and planned expansion sample sizes if relevant conditions are identified. (If applicable) b)
: A list of the standards and/or requirements that will be used to evaluate indications identified during nondestructive examination of the reactor vessel Attachment 2 head (e.g., the specific industry or procedural standards which will be used to evaluate potential leakage and/or flaw indications). A.3 Boric Acid Corrosion Control Program a)
: Copy of the procedures that govern the scope, equipment and implementation of the inspections required to identify boric acid leakage and the procedures for boric acid leakage/corrosion evaluation. b) Please provide a list of leaks (including Code class of the components) that have been identified since the last refueling outage and associated corrective action documentation.
: If during the last cycle, the unit was shutdown, please provide documentation of containment walkdown inspections performed as part of the boric acid corrosion control program. c) Please provide a copy of the most recent self-assessment performed for the boric acid corrosion control program. A.4 Steam Generator Tube Inspections a) A detailed schedule of: i)
: Steam generator tube inspection, data analyses, and repair activities for the upcoming outage  ii)
: Steam generator secondary side inspection activities for the upcoming outage. b) Please provide a copy of your steam generator inservice inspection program and plan.
: Please include a copy of the operational assessment from last outage and a copy of the following documents as they become available:  i) Degradation assessment ii) Condition monitoring assessment  c) If you are planning on modifying your Technical Specifications such that they are consistent with Technical Specification Task Force Traveler
: TSTF-449, "Steam Generator Tube Integrity," please provide copies of your correspondence with the NRC regarding deviations from the standard technical specifications. d) Copy of steam generator history documentation given to vendors performing eddy current testing of the steam generators during the upcoming outage. e) Copy of steam generator eddy current data analyst guidelines and site validated eddy current technique specification sheets.
: Additionally, please provide a copy of EPRI Appendix H, "Examination Technique Specification Sheets," qualification records.
: Attachment 2 f) Identify and quantify any steam generator tube leakage experienced during the previous operating cycle.
: Also provide documentation identifying which steam generator was leaking and corrective actions completed or planned for this condition (If applicable). g)
: Provide past history of the condition and issues pertaining to the secondary side of the steam generators (including items such as loose parts, fouling, top of tube sheet condition, crud removal amounts, etc.) h) Provide copies of your most recent self assessments of the steam generator monitoring, loose parts monitoring, and secondary side water chemistry control programs. i) Indicate where the primary, secondary, and resolution analyses are scheduled to take place. j) Provide a summary of the scope of the steam generator tube examinations, including examination methods such as Bobbin, Rotating Pancake, or Plus Point, and the percentage of tubes to be examined. Do not provide these documents separately if already included in other information requested. A.5 Additional Information Related to all Inservice Inspection Activities a)
: A list with a brief description of inservice inspection, boric acid corrosion control program, and steam generator tube inspection related issues (e.g., condition reports) entered into your corrective action program since the beginning of the last refueling outage (for Unit 1).
: For example, a list based upon data base searches using key words related to piping or steam generator tube degradation such as: inservice inspection, ASME Code, Section XI, NDE, cracks, wear, thinning, leakage, rust, corrosion, boric acid, or errors in piping/steam generator tube examinations. b)
: Please provide names and phone numbers for the following program leads: Inservice inspection (examination, planning)
: Containment exams Reactor pressure vessel head exams Snubbers and supports Repair and replacement program
: Licensing
: Site welding engineer Boric acid corrosion control program Attachment 2
: Steam generator inspection activities (site lead and vendor contact) c) Please provide a copy of NDE procedures, the boric acid corrosion control program and related procedures, and the welding program. B. Information to be Provided Onsite to the Inspector(s) at the Entrance Meeting (April 1, 2013): B.1 Inservice Inspection / Welding Programs and Schedule Information a) Updated schedules for inservice inspection/nondestructive examination activities, including steam generator tube inspections, planned welding activities, and schedule showing contingency repair plans, if available. b) For ASME Code Class 1 and 2 welds selected by the inspector from the lists provided from section A of this enclosure, please provide copies of the following documentation for each subject weld: i) Weld data sheet (traveler)
ii) Weld configuration and system location iii) Applicable Code Edition and Addenda for weldment iv) Applicable Code Edition and Addenda for welding procedures
v) Applicable weld procedures used to fabricate the welds vi) Copies of procedure qualification records supporting the weld procedures from B.1.b.v vii) Copies of mechanical test reports identified in the procedure qualification records above viii) Copies of the nonconformance reports for the selected welds (If applicable) ix) Radiographs of the selected welds and access to equipment to allow viewing radiographs (If radiographic testing was performed) x) Copies of the preservice examination records for the selected welds xi) Copies of welder performance qualifications records applicable to the selected welds, including documentation that welder maintained proficiency in the applicable welding processes specified in the weld procedures (at least 6 months prior to the date of subject work) xii) Copies of nondestructive examination personnel qualifications (Visual inspection, penetrant testing, ultrasonic testing, radiographic testing), as applicable Attachment 2 c) For the inservice inspection related corrective action issues selected by the inspectors from section A of this enclosure, provide a copy of the corrective actions and supporting documentation. d) For the nondestructive examination reports with relevant conditions on Code Class 1 and 2 systems selected by the inspectors from Section A above, provide a copy of the examination records, examiner qualification records, and associated corrective action documents. e) A copy of (or ready access to) most current revision of the inservice inspection program manual and plan for the current Interval. f) For the nondestructive examinations selected by the inspectors from section A of this enclosure, provide a copy of the nondestructive examination procedures used to perform the examinations (including calibration and flaw characterization/sizing procedures).
: For ultrasonic examination procedures qualified in accordance with ASME Section XI, Appendix VIII, provide documentation supporting the procedure qualification (e.g., the EPRI performance demonstration qualification summary sheets).
: Also, include qualification documentation of the specific equipment to be used (e.g., ultrasonic unit, cables, and transducers including serial numbers) and nondestructive examination personnel qualification records. B.2 Reactor Pressure Vessel Head  a) Provide the nondestructive personnel qualification records for the examiners who will perform examinations of the reactor pressure vessel head. b) Provide drawings showing the following: (If a visual examination is planned for the upcoming refueling outage) i) Reactor pressure vessel head and control rod drive mechanism nozzle configurations ii) Reactor pressure vessel head insulation configuration
: Note: The drawings listed above should include fabrication drawings for the nozzle attachment welds as applicable. c) Copy of nondestructive examination reports from the last reactor pressure vessel head examination. d) Copy of evaluation or calculation demonstrating that the scope of the visual examination of the upper head will meet the 95 percent minimum coverage required by NRC Order
: EA-03-009 (If a visual examination is planned for the upcoming refueling outage). e) Provide a copy of the procedures that will be used to identify the source of any boric acid deposits identified on the reactor pressure vessel head.
: If no explicit Attachment 2 procedures exist which govern this activity, provide a description of the process to be followed including personnel responsibilities and expectations. f)
: Provide a copy of the updated calculation of effective degradation years for the reactor pressure vessel head susceptibility ranking. g)
: Provide copy of the vendor qualification report(s) that demonstrates the detection capability of the nondestructive examination equipment used for the reactor pressure vessel head examinations.
: Also, identify any changes in equipment configurations used for the reactor pressure vessel head examinations which differ from that used in the vendor qualification report(s). B.3 Boric Acid Corrosion Control Program  a) Please provide boric acid walkdown inspection results, an updated list of boric acid leaks identified so far this outage, associated corrective action documentation, and overall status of planned boric acid inspections. b) Please provide any engineering evaluations completed for boric acid leaks identified since the end of the last refueling outage.
: Please include a status of corrective actions to repair and/or clean these boric acid leaks.
: Please identify specifically which known leaks, if any, have remained in service or will remain in service as active leaks.
: B.4 Steam Generator Tube Inspections a) Copies of the Examination Technique Specification Sheets and associated justification for any revisions. b) Copy of the guidance to be followed if a loose part or foreign material is identified in the steam generators. c) Please provide a copy of the eddy current testing procedures used to perform the steam generator tube inspections (specifically calibration and flaw characterization/sizing procedures, etc.).
: Also include documentation for the specific equipment to be used. d) Please provide copies of your responses to NRC and industry operating experience communications such as Generic Letters, Information Notices, etc.
(as applicable to steam generator tube inspections) Do not provide these documents separately if already included in other information requested such as the degradation assessment. e) List of corrective action documents generated by the vendor and/or site with respect to steam generator inspection activities.
: Attachment 2 B.5 Codes and Standards a) Ready access to (i.e., copies provided to the inspector(s) for use during the inspection at the onsite inspection location, or room number and location where available): i)
: Applicable Editions of the ASME Code (Sections V, IX, and XI) for the inservice inspection program and the repair/replacement program. ii)
: EPRI and industry standards referenced in the procedures used to perform the steam generator tube eddy current examination.
: Inspector Contact Information: Jim Drake Senior Reactor Inspector
: 817-200-1558
: James.Drake@nrc.gov Mailing Address:
: US NRC Region IV
: Attn: Jim Drake 1600 Lamar Blvd Arlington, TX 76011
}}
}}

Latest revision as of 15:34, 20 December 2019

IR 05000313-13-003, 05000368-13-003; 04/01/2013 - 06/30/2013; Arkansas Nuclear One, Units 1 and 2, Integrated Resident and Regional Report; Surveillance Testing, Event Follow-up
ML13225A747
Person / Time
Site: Arkansas Nuclear  Entergy icon.png
Issue date: 08/13/2013
From: Allen D
NRC/RGN-IV/DRP/RPB-E
To: Jeremy G. Browning
Entergy Operations
Allen D
References
IR-13-003
Download: ML13225A747 (55)


Text

UNITED STATE S NUC LEAR REGULATOR Y C OMMI SSI ON ust 13, 2013

SUBJECT:

ARKANSAS NUCLEAR ONE - NRC INTEGRATED INSPECTION REPORT 05000313/2013003 AND 05000368/2013003

Dear Mr. Browning:

On June 30, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Arkansas Nuclear One Station Units 1 and 2, facility. The enclosed inspection report documents the inspection results which were discussed on July 2, 2013, with you and other members of your staff.

The inspections examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

One NRC identified and one self-revealing finding of very low safety significance (Green) were identified during this inspection. Both of these findings were determined to involve violations of NRC requirements. The NRC is treating these violations as non-cited violations (NCVs)

consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest these non-cited violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Arkansas Nuclear One.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV; and the NRC Resident Inspector at Arkansas Nuclear One.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's Agencywide Document Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Donald B. Allen, Chief Project Branch E Division of Reactor Projects Docket Nos.: 05000313, 05000368 License Nos: DPR-51; NPF-6

Enclosure:

Inspection Report 05000313/2013003 and 05000368/2013003 w/ Attachments: 1. Supplemental Information 2. Request for Information for the Inservice Inspection

REGION IV==

Docket: 05000313, 05000368 License: DPR-51, NPF-6 Report: 05000313/2013003, 05000368/2013003 Licensee: Entergy Operations Inc.

Facility: Arkansas Nuclear One, Units 1 and 2 Location: Junction of Hwy. 64 West and Hwy. 333 South Russellville, Arkansas Dates: April 1 through June 30, 2013 Inspectors: A. Sanchez, Senior Resident Inspector B. Tindell, Senior Resident Inspector A. Fairbanks, Resident Inspector W. Schaup, Resident Inspector R. Azua, Senior Project Engineer I. Anchondo, Senior Reactor Inspector D. Bradley, Project Engineer J. Melfi, Project Engineer Approved By: Don Allen, Chief, Project Branch E Division of Reactor Projects-1- Enclosure

SUMMARY OF FINDINGS

IR 05000313/2013003, 05000368/2013003; 04/01/2013 - 06/30/2013; Arkansas Nuclear One,

Units 1 and 2, Integrated Resident and Regional Report; Surveillance Testing, Event Followup.

The report covered a 3-month period of inspection by resident inspectors and an announced baseline inspection by region-based inspectors. Two Green non-cited violations were identified.

The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter 0609, Significance Determination Process. The cross-cutting aspect is determined using Inspection Manual Chapter 0310, Components Within the Cross-Cutting Areas. Findings for which the significance determination process does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

NRC-Identified Findings and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green.

Inspectors documented a Green self-revealing non-cited violation of Technical Specification 6.4.1.a for the licensees failure to implement procedures recommended by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.

Specifically, the licensee failed to follow procedures for the replacement of the supply breaker for control room emergency chiller 2VE-1A. As a result, the breaker was installed incorrectly and the chiller was inoperable for over two months. Immediate corrective actions included proper installation of the breaker and procedural requirements for visual verification of breaker configuration. The licensee documented the issue in their corrective action program as CR-ANO-2-2013-00233.

Inspectors concluded that the failure to follow Procedure 1403.179 for replacement of the train A control room emergency chiller breaker is a performance deficiency.

The performance deficiency is more than minor because it was associated with the human performance attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences, and is therefore a finding. Specifically, the loose breaker connection adversely affected the availability and reliability of the control room emergency chiller A. Using Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, and Appendix A, The Significance Determination Process (SDP) for Findings at Power, the inspectors determined that the finding required a detailed risk evaluation because it represented an actual loss of function of a single train for longer than its technical specification allowed outage time. The senior reactor analyst performed a detailed risk evaluation using the Arkansas Nuclear One Standardized Plant Analysis Risk models. The dominant risk sequences include a seismically-induced loss of offsite power with the failure of control room emergency chiller A. The analyst assumed that the operators and control room instrumentation could survive a peak control room temperature of 120° F, and that chiller A was susceptible to failure during a seismic event for the 83 days. None of the core damage sequences affected by this performance deficiency were important to the large, early release frequency.

Therefore, based on the combined internal and seismic ICCDP of 2.9 x 10-7, this finding was of very low safety significance (Green). The finding was determined to have a cross-cutting aspect in the area of human performance, associated with work practices, in that the licensee failed to use work practices that support human performance. Specifically, licensee personnel were aware of the possibility of misaligning the wire grip style lug, but failed to use adequate self and peer checking to ensure the lug was correctly installed H.4(a) (Section 4OA3).

Cornerstone: Barrier Integrity

Green.

The inspectors identified a non-cited violation of Unit 2 Technical Specification 6.5.16, Containment Leakage Rate Testing Program, for the failure to evaluate and take appropriate corrective actions to achieve acceptable performance for containment isolation valves that exceed the local leak rate administrative limit.

The licensee entered this issue into the corrective action program as Condition Report CR-ANO-2-2013-01370.

The failure to perform a cause determination and take appropriate corrective actions for containment isolation valves that exceed the local leak rate administrative limit was a performance deficiency. The performance deficiency was more than minor because it was associated with the procedure quality attribute of the Barrier Integrity Cornerstone and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events, and is therefore a finding.

Specifically, the failure to perform a cause determination and take appropriate corrective actions adversely affected the licensee's ability to ensure containment isolation valves function properly. Using Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, and Appendix A, The Significance Determination Process (SDP) for Findings at Power, the finding is determined to have very low safety significance because it did not represent an actual open pathway in the physical integrity of reactor containment, containment isolation system, or heat removal components, and the finding did not involve an actual reduction in function of hydrogen igniters in the reactor containment. Since the cause of the performance deficiency occurred more than three years ago, the inspectors concluded that the finding was not representative of current licensee performance and no cross-cutting aspect was assigned (Section 1R22).

Licensee-Identified Violations

None

PLANT STATUS

Unit 1 began the period in refueling outage 1R24 and remained shut down for the entire inspection period as the licensee recovered from the main generator stator drop that occurred on March 31, 2013.

Unit 2 began the period in a forced outage due to the Unit 1 main generator stator drop. On April 28, 2013, operators performed a reactor startup and closed the main generator output breakers, placing Unit 2 on the grid. Unit 2 reached 100 percent power on April 30, 2013 and remained there for the rest of the period.

REPORT DETAILS

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

Summer Readiness for Offsite and Alternate ac Power Systems

a. Inspection Scope

The inspectors performed a review of preparations for summer weather for selected systems, including conditions that could lead to loss-of-offsite power and conditions that could result from high temperatures. The inspectors reviewed the procedures affecting these areas and the communications protocols between the transmission system operator and the plant to verify that the appropriate information was being exchanged when issues arose that could affect the offsite power system. Examples of aspects considered in the inspectors review included:

  • The coordination between the transmission system operator and the plants operations personnel during off-normal or emergency events
  • The explanations for the events
  • The estimates of when the offsite power system would be returned to a normal state
  • The notifications from the transmission system operator to the plant when the offsite power system was returned to normal During the inspection, the inspectors focused on plant-specific design features and the procedures used by plant personnel to mitigate or respond to adverse weather conditions. Additionally, the inspectors reviewed the Safety Analysis Report and performance requirements for systems selected for inspection, and verified that operator actions were appropriate as specified by plant-specific procedures. Specific documents

reviewed during this inspection are listed in the attachment. The inspectors also reviewed corrective action program items to verify that the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their corrective action program in accordance with station corrective action procedures. The inspectors reviews focused specifically on the following plant systems:

  • Startup transformers
  • Vital buses

b. Findings

No findings were identified.

1R04 Equipment Alignment

Partial Walkdown

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant systems:

  • June 5, 2013, Unit 2, high pressure safety injection pumps A and C while high pressure safety injection pump B was unavailable for planned maintenance
  • June 6, 2013, Unit 1, emergency diesel generator A while emergency diesel generator B was unavailable for planned maintenance The inspectors selected the systems based on their risk significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors focused on any discrepancies that could affect the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, the Safety Analysis Report, technical specification requirements, administrative technical specifications, outstanding work orders, condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also inspected accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program with

the appropriate significance characterization. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of two partial system walkdown samples as defined in Inspection Procedure 71111.04-05.

b. Findings

No findings were identified.

1R05 Fire Protection

Quarterly Fire Inspection Tours

a. Inspection Scope

The inspectors conducted fire protection walkdowns in the following risk-significant plant areas:

  • June 25, 2013, Unit 1, Fire Zone 95-O, north battery room
  • June 25, 2013, Unit 2, Fire Zone 2098-L, cable spreading room
  • June 25, 2013, Unit 2, Fire Zone NA, intake structure
  • June 26, 2013, Unit 1, Fire Zone 170-Z, steam pipe area The inspectors reviewed areas to assess if licensee personnel had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant; effectively maintained fire detection and suppression capability; maintained passive fire protection features in good material condition; and had implemented adequate compensatory measures for out of service, degraded or inoperable fire protection equipment, systems, or features, in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants individual plant examination of external events with later additional insights, their potential to affect equipment that could initiate or mitigate a plant transient, or their impact on the plants ability to respond to a security event. Using the documents listed in the attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four quarterly fire-protection inspection samples as defined in Inspection Procedure 71111.05-05.

b. Findings

No findings were identified.

1R06 Flood Protection Measures

a. Inspection Scope

The inspectors reviewed the Safety Analysis Report, the flooding analysis, and plant procedures to assess susceptibilities involving internal flooding; reviewed the corrective action program to determine if licensee personnel identified and corrected flooding problems; and verified that operator actions for coping with flooding can reasonably achieve the desired outcomes. The inspectors also inspected the areas listed below to verify the adequacy of equipment seals located below the flood line, floor and wall penetration seals, watertight door seals, common drain lines and sumps, sump pumps, level alarms, and control circuits, and temporary or removable flood barriers. Specific documents reviewed during this inspection are listed in the attachment.

  • May 24, 2013, Units 1 and 2, intake structures, 366 foot level These activities constitute completion of one flood protection measures inspection sample as defined in Inspection Procedure 71111.06-05.

b. Findings

No findings were identified.

1R08 Inservice Inspection Activities

Completion of Sections

.1 through .5, below, constitutes completion of one sample as

defined in Inspection Procedure 71111.08-05.

.1 Inspection Activities Other Than Steam Generator Tube Inspection, Pressurized Water

Reactor Vessel Upper Head Penetration Inspections, and Boric Acid Corrosion Control (71111.08-02.01)

a. Inspection Scope

The inspectors observed four nondestructive examination activities and reviewed four nondestructive examination activities that included three types of examinations. The licensee did not identify any relevant indications accepted for continued service during the nondestructive examinations.

The inspectors directly observed the following nondestructive examinations:

SYSTEM WELD IDENTIFICATION EXAMINATION TYPE Reactor Coolant Pressurizer Relief Nozzle Ultrasonic System Between W-X Axis (Report No. 1-ISI-UT-13-017)

SYSTEM WELD IDENTIFICATION EXAMINATION TYPE Reactor Coolant Cold Leg Drain Nozzle to SE Circ Weld Ultrasonic System (Report No. 1-ISI-UT-13-020)

Main Steam EBB-3-MS-143, I.W.A Magnetic Particle (Report No. 1-ISI-MT-13-001)

Building Spray HCD-8/BS-123 Visual (VT-3)

(Report No. 1-ISI-VT-13-042)

The inspectors reviewed records for the following nondestructive examinations:

SYSTEM WELD IDENTIFICATION EXAMINATION TYPE Reactor Coolant Pipe-to-pipe weld Ultrasonic System (Report No. 1-ISI-UT-13-021)

Reactor Coolant Pipe-to-Cap weld Radiographic System (Report No.1-BOP-RT-13-011)

Reactor Coolant Reducer-to-Flange weld Radiographic System (Report No.1-BOP-RT-13-0070)

Reactor Coolant Pipe-to-elbow weld Radiographic System (Report No. 1-BOP-RT-13-012)

During the review and observation of each examination, the inspectors verified that activities were performed in accordance with the American Society of Mechanical Engineers (ASME) code requirements and applicable procedures. The inspectors also verified the qualifications of all nondestructive examination technicians performing the inspections were current.

These actions constitute completion of the requirements for Section 02.01.

b. Findings

No findings were identified.

.2 Vessel Upper Head Penetration Inspection Activities (71111.08-02.02)

a. Inspection Scope

No reactor vessel head inspections were performed during this outage.

b. Findings

No findings were identified.

.3 Boric Acid Corrosion Control Inspection Activities (71111.08-02.03)

a. Inspection Scope

The inspectors evaluated the implementation of the licensees boric acid corrosion control program for monitoring degradation of those systems that could be adversely affected by boric acid corrosion. The inspectors reviewed the documentation associated with the licensees boric acid corrosion control walkdown as specified in Procedures SEP-BAC-ANO-001, Boric Acid Corrosion Control Program Inspection and Identification of Boric Acid Leaks for ANO-1 and ANO-2, Revision 0, CEP-BAC-001, Boric Acid Corrosion Control (BACC) Program Plan, Revision 0, and EN-DC-319, Inspection and Evaluation of Boric Acid Leaks, Revision 8. The inspectors also reviewed the visual records of the components and equipment. The inspectors verified that the visual inspections emphasized locations where boric acid leaks could cause degradation of safety-significant components. The inspectors also verified that the engineering evaluations for those components where boric acid was identified gave assurance that the ASME code wall thickness limits were properly maintained. The inspectors confirmed that the corrective actions performed for evidence of boric acid leaks were consistent with requirements of the ASME code. Specific documents reviewed during this inspection are listed in the attachment.

These actions constitute completion of the requirements for Section 02.03.

b. Findings

No findings were identified.

.4 Steam Generator Tube Inspection Activities (71111.08-02.04)

a. Inspection Scope

The licensee performed steam generator inspection activities during refueling outage 1R24 to determine the extent of bowing and tube-to-tube wear progression.

The activities were not technical specification required inspections. The scope of the licensees eddy current testing included:

  • Bobbin testing of 454 tubes in steam generator A from tube support 09S to upper tube end.
  • Bobbin testing of 446 tubes in steam generator B from tube support 09S to upper tube end.
  • Full length eddy current array probe (X-probe) of 304 tubes in steam generator A (including 17 proximity tubes).
  • Full length eddy current array probe (X-probe) of 308 tubes in steam generator B (including 14 proximity tubes).
  • Full length eddy current array probe (X-probe) of 48 tubes in steam generator A exhibiting tube-to-tube wear.
  • Full length eddy current array probe (X-probe) of 74 tubes in steam generator B exhibiting tube-to-tube wear.
  • Full length eddy current array probe (X-probe) of 51 tubes in steam generator A with prior proximity signals (PRX).
  • Full length eddy current array probe (X-probe) of 17 tubes in steam generator B with prior proximity signals (PRX).

The following tube degradation mechanisms were identified:

  • Wear at the tube support plate intersections.
  • Tube-to-tube wear.

The inspectors observed portions of the eddy current testing being performed and verified that:

(1) the appropriate probes were used for identifying the expected types of degradation,
(2) calibration requirements were adhered to, and
(3) probe travel speed was in accordance with procedural requirements. The inspectors performed a review of the site-specific qualifications for the techniques being used, and verified that eddy current test data analyses were adequately performed per Electric Power Research Institute and site specific guidelines.

Finally, the inspectors review selected eddy current test data and verified that the analytical techniques used were adequate.

These actions constitute completion of the requirements for Section 02.04.

b. Findings

No findings were identified.

.5 Identification and Resolution of Problems (71111.08-02.05)

a. Inspection Scope

The inspectors reviewed 13 condition reports associated with inservice inspection activities, and determined that the corrective actions taken were appropriate. The inspectors concluded that the licensee had an appropriate threshold for entering inservice inspection issues into the corrective action program and had procedures that direct a root cause evaluation when necessary. The licensee also had an effective program for applying inservice inspection industry operating experience. Specific documents reviewed during this inspection are listed in the attachment.

These actions constitute completion of the requirements of Section 02.05.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

.1 Quarterly Review of Licensed Operator Requalification Program

a. Inspection Scope

On June 26, 2013, the inspectors observed Units 1 and 2 licensed operators in the plant during requalification testing job performance measures. The inspectors assessed the following areas:

  • Licensed operator performance
  • The ability of the licensee to administer the evaluations
  • Follow-up actions taken by the licensee for identified discrepancies These activities constitute completion of two quarterly licensed operator requalification program samples as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

.2 Quarterly Observation of Licensed Operator Performance

a. Inspection Scope

The inspectors observed the performance of on-shift licensed operators in the plants main control room. The inspectors assessed the operators adherence to plant procedures, including conduct of operations procedures and other operations

department policies. The inspectors observed the operators performance during the following periods of heightened activities:

  • April 28, 2013, Unit 2, reactor startup
  • June 18, 2013, Unit 1, train B undervoltage surveillances These activities constitute completion of two quarterly licensed operator performance samples as defined in Inspection Procedure 71111.11-05.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk significant systems:

  • June 10, 2013, Unit 2, high pressure safety injection B flow control valve 480 Volt breaker replacement The inspectors reviewed events where ineffective equipment maintenance had resulted in failures and independently verified the licensee's actions to address system performance or problems in terms of the following:
  • Implementing appropriate work practices
  • Identifying and addressing common cause failures
  • Characterizing system reliability issues for performance
  • Charging unavailability for performance
  • Trending key parameters for condition monitoring
  • Establishing appropriate performance criteria
  • Establishing appropriate and adequate goals and corrective actions The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the corrective action program with the appropriate significance characterization. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of two maintenance effectiveness samples as defined in Inspection Procedure 71111.12-05.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed licensee personnel's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:

  • January 9, 2013, Units 1 and 2, heavy equipment driving in the switchyard
  • March 31, 2013, Units 1 and 2, Bigge lift rig collapse and generator stator drop
  • April 11, 2013, Unit 1, reactor building hatch open during tornado warning
  • April 23, 2013, Unit 1, outage activities following the main generator stator drop
  • May 4, 2013, Units 1 and 2, dropped stator and damaged carriage removal
  • May 20, 2013, Units 1 and 2, heavy equipment in train bay The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)and that the assessments were accurate and complete. When licensee personnel performed emergent work, the inspectors verified that the licensee personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed the technical specification requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of seven maintenance risk assessments and emergent work control inspection samples as defined in Inspection Procedure 71111.13-05.

b. Findings

No findings were identified.

1R15 Operability Evaluations and Functionality Assessments

a. Inspection Scope

The inspectors reviewed the following issues:

  • December 5, 2012, Units 1 and 2, startup transformer 2 sudden pressure relays wetting during design basis flood
  • April 11, 2013, Unit 1, reactor building pipe support EBB-6-H13 not fully engaged
  • April 24, 2013, Unit 2, debris identified in containment during closeout
  • June 7, 2013, Unit 2, wetting of emergency diesel generator B fuel oil transfer pump The inspectors selected these operability and functionality issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure technical specification operability was properly justified and to verify the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the technical specifications and Safety Analysis Report to the licensees evaluations to determine whether the components or systems were operable or functional. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. Additionally, the inspectors reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of six operability evaluations inspection samples as defined in Inspection Procedure 71111.15-05.

b. Findings

No findings were identified.

1R18 Plant Modifications

Temporary Modifications

a. Inspection Scope

To verify that the safety functions of important safety systems were not degraded, The inspectors reviewed the following temporary modifications:

  • April 23, 2013, Unit 1, source range nuclear instrument NI-501 modification for fuel movement
  • April 15, 2013, Unit 1, startup transformer 1 temporary power supply to vital buses A3 and A4
  • April 15, 2013, Unit 1, startup transformer 2 temporary power supply to vital buses A3 and A4 buses through temporary switchgear The inspectors reviewed the temporary modifications and the associated safety-evaluation screening against the system design bases documentation, including the Safety Analysis Report and the technical specifications, and verified that the modification did not adversely affect the system operability or availability. The inspectors also verified that the installation and restoration were consistent with the modification documents and that configuration control was adequate. Additionally, the inspectors verified that the temporary modification was identified on control room drawings, appropriate tags were placed on the affected equipment, and licensee personnel evaluated the combined effects on mitigating systems and the integrity of radiological barriers. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of three samples for temporary plant modifications, as defined in Inspection Procedure 71111.18-05.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the following post-maintenance activities to verify that test activities were adequate to ensure system operability and functional capability:

  • May 21, 2013, Unit 2, main steam supply valve CV-1000-1, from steam generator A to emergency feedwater pump turbine 2K-3, following cleaning, inspection, and lubrication of actuator and meggering of the motor
  • June 6, 2013, Unit 1, VCH-4B, vital switchgear emergency chiller B, following planned maintenance
  • June 13, 2013, Unit 1, P-35A, reactor building spray pump A , following bearing and seal replacement
  • April 23, 2013, Alternate AC Diesel Generator Bus 2A9 and the Alternate AC Diesel Generator Following Repairs from the Unit 1 Dropped Stator Event The inspectors selected these activities based upon the structure, system, or component's ability to affect risk. The inspectors evaluated these activities to verify that the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; and test instrumentation was appropriate.

The inspectors evaluated the activities against the technical specifications, the Safety Analysis Report, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with post-maintenance tests to determine whether the licensee was identifying problems and entering them in the corrective action program and that the problems were being corrected commensurate with their importance to safety. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of five post-maintenance testing inspection samples as defined in Inspection Procedure 71111.19-05.

b. Findings

No findings were identified.

1R20 Refueling and Other Outage Activities

a. Inspection Scope

The inspectors reviewed the outage safety plan and contingency plans for the Unit 1 refueling outage and the Unit 2 forced outage, to confirm that licensee personnel had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing a plan that assured maintenance of defense in depth.

During the refueling and forced outages, the inspectors monitored licensee controls over the outage activities listed below, as applicable.

  • Configuration management, including maintenance of defense in depth, is commensurate with the outage safety plan for key safety functions and compliance with the applicable technical specifications when taking equipment out of service
  • Clearance activities, including confirmation that tags were properly hung and equipment appropriately configured to safely support the work or testing
  • Installation and configuration of reactor coolant pressure, level, and temperature instruments to provide accurate indication, accounting for instrument error
  • Status and configuration of electrical systems to ensure that technical specifications and outage safety-plan requirements were met, and controls over switchyard activities
  • Verification that outage work was not impacting the ability of the operators to operate the spent fuel pool cooling system
  • Reactor water inventory controls, including flow paths, configurations, and alternative means for inventory addition, and controls to prevent inventory loss
  • Controls over activities that could affect reactivity
  • Refueling activities, including fuel handling
  • Startup and ascension to full power operation, tracking of startup prerequisites, walkdown of the containment to verify that debris had not been left which could block emergency core cooling system suction strainers
  • Licensee identification and resolution of problems related to refueling outage activities Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one refueling outage and one other outage inspection samples, as defined in Inspection Procedure 71111.20-05.

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the Safety Analysis Report, procedure requirements, and technical specifications to ensure that the surveillance activities listed below demonstrated that the systems, structures, and/or components tested were capable of performing their intended safety functions. The inspectors either witnessed or reviewed test data to verify that the significant surveillance test attributes were adequate to address the following:

  • Preconditioning
  • Evaluation of testing impact on the plant
  • Acceptance criteria
  • Test equipment
  • Procedures
  • Jumper/lifted lead controls
  • Test data
  • Testing frequency and method demonstrated technical specification operability
  • Test equipment removal
  • Restoration of plant systems
  • Fulfillment of ASME Code requirements
  • Updating of performance indicator data
  • Engineering evaluations and root causes
  • Reference setting data
  • Annunciators and alarms setpoints The inspectors also verified that licensee personnel identified and implemented any needed corrective actions associated with the surveillance testing.
  • September 24, 2012, Unit 2, letdown isolation valve 2CV-4832-2 local leak rate test
  • February 10, 2013, Units 1 and 2, alternate ac diesel generator quarterly test
  • May 1, 2013, Unit 2, remote pressurizer proportional heater test
  • May 22, 2013, Unit 2, emergency feedwater pump A inservice test
  • May 29, 2013, Unit 2, emergency diesel generator A monthly test Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of five surveillance testing inspection samples (one pump or valve inservice test sample, one containment isolation valve test sample,

and three routine surveillance testing samples) as defined in Inspection Procedure 71111.22-05.

b. Findings

Introduction.

The inspectors identified a Green non-cited violation of Unit 2 Technical Specification 6.5.16, Containment Leakage Rate Testing Program, for the failure to evaluate and take appropriate corrective actions to achieve acceptable performance for containment isolation valves that exceed the local leak rate administrative limit.

Description.

On February 28, 2011, letdown isolation valve 2CV-4823-2 exceeded the local leak rate administrative limit, which was documented in CR-ANO-2-2011-00800.

Work was scheduled to be performed on the air operator for the valve; however, no valve seat work was planned or performed. On March 11, 2011, after completion of work on the air operator, the valve exceeded the local leak rate administrative limit. The licensee generated a condition report that was closed to the work order process without a cause evaluation or corrective actions. On September 24, 2012, the valve again exceeded the as-found local leak rate administrative limit, which was documented in CR-ANO-2-2012-02270. The response stated that there were no programmatic requirements and no technical specification implications relative to containment integrity and/or leakage as a result of the leakage from valve 2CV-4823-2 exceeding its administrative limit; therefore, the leak rate from valve 2CV-4823-2 was acceptable. The inspectors noted that the valve was scheduled for repair in the spring of 2014.

The inspectors independently reviewed Unit 2 Technical Specification 6.5.16, Containment Leakage Rate Testing Program and determined that the licensees program is required to implement Nuclear Energy Institute 94-01, Industry Guideline for Implementing Performance-Based Option of 10 CFR Part 50, Appendix J, Revision 2-A.

The standard states, in part, that a cause determination should be performed and corrective actions identified that focus on those activities that can eliminate the identified cause of a failure with appropriate steps to eliminate recurrence. A failure, as defined by the standard, is exceeding an administrative limit and not the total failure of the valve.

The inspectors reviewed the licensees corrective action program documents and their containment leakage rate testing program documents, and determined that they did not meet the technical specification required guidance. Specifically, the licensees programs did not specify that a cause determination be performed for conditions where containment isolation valves exceed their administrative limits. In addition, there was no guidance to ensure that corrective actions address the cause of the failure. The inspectors also noted that the licensee was not treating these items as degraded conditions to ensure that they were corrected in a timely manner. Based on the above and the licensees statements that the leakage from 2CF-4823-2 was acceptable, the inspectors concluded that the licensee had not adequately implemented Nuclear Energy Institute 94-01, as required by Technical Specification 6.5.16.

The inspectors concluded that because the licensees program was established more than three years ago, the failure to adequately implement the guidance was not representative of current licensee performance.

Analysis.

The failure to perform a cause determination and take appropriate corrective actions for containment isolation valves that exceed the local leak rate administrative limit is a performance deficiency. The performance deficiency is more than minor because it was associated with the procedure quality attribute of the Barrier Integrity Cornerstone and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events, and is therefore a finding. Specifically, the failure to perform a cause determination and take appropriate corrective actions adversely affected the licensee's ability to ensure containment isolation valves function properly.

Using Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, and Appendix A, The Significance Determination Process (SDP) for Findings at Power, the finding is determined to have very low safety significance because it did not represent an actual open pathway in the physical integrity of reactor containment, containment isolation system, or heat removal components, and the finding did not involve an actual reduction in function of hydrogen igniters in the reactor containment. Since the cause of the performance deficiency occurred more than three years ago, the inspectors concluded that the finding was not representative of current licensee performance and no cross-cutting aspect was assigned.

Enforcement.

Unit 2 Technical Specification 6.5.16, Containment Leakage Rate Testing Program, states, in part, that a program shall be established to implement the leakage rate testing of the containment as required by 10 CFR Part 50, Appendix J, Option B, Performance-Based Requirements. This program shall be in accordance with the guidelines contained in Regulatory Guide 1.163, Performance-Based Containment Leak-Test Program, dated September 1995. Regulatory Guide 1.163, Section C, Regulatory Position, further states, in part, that NEI 94-01, Revision 0, dated July 26, 1995, Industry Guideline for Implementing Performance Based Option of 10 CFR 50, Appendix J provides methods for complying with the provisions of Option B in Appendix J to 10 CFR Part 50. Contrary to the above, as of June 30, 2013, the licensee failed to implement a program for leakage rate testing of the containment in accordance with Technical Specification 6.5.16. Specifically, Nuclear Energy Institute 94-01, Section 10.2.3.4, states, in part, that if test results are not acceptable, then a cause determination should be performed and corrective actions identified that focus on those activities that can eliminate the identified cause of the failure. A failure, as defined by the standard, is exceeding an administrative limit and not the total failure of the valve. However, the licensees program for containment leakage rate testing did not require a cause determination and identification of corrective actions to eliminate the cause of the failure. The licensee documented this failure in Condition Report CR-ANO-2-2013-01370. Because this finding is of very low safety significance and has been entered into the corrective action program, this violation is being treated as a non-cited violation consistent with Section 2.3.2.a of the NRC Enforcement Policy:

NCV 05000368/2013003-01, Failure to Evaluate and Correct Excessive Containment Isolation Valve Leakage.

OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection

4OA1 Performance Indicator Verification

.1 Data Submission Issue

a. Inspection Scope

The inspectors performed a review of the performance indicator data submitted by the licensee for the first quarter 2013 performance indicators for any obvious inconsistencies prior to its public release in accordance with Inspection Manual Chapter 0608, Performance Indicator Program.

This review was performed as part of the inspectors normal plant status activities and, as such, did not constitute a separate inspection sample.

b. Findings

No findings were identified.

.2 Safety System Functional Failures (MS05)

a. Inspection Scope

The inspectors sampled licensee submittals for the safety system functional failures performance indicator for both Units 1 and 2 for the period from the first quarter 2012 through the first quarter 2013. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, and NUREG-1022, Event Reporting Guidelines 10 CFR 50.72 and 50.73." The inspectors reviewed the licensees operator narrative logs, operability assessments, maintenance rule records, maintenance work orders, issue reports, event reports, and NRC integrated inspection reports for the period of January 2012 through March 2013, to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report.

These activities constitute completion of two safety system functional failures samples as defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

.3 Reactor Coolant System Specific Activity (BI01)

a. Inspection Scope

The inspectors sampled licensee submittals for the reactor coolant system specific activity performance indicator for both Units 1 and 2 for the period from the second quarter 2012 through the first quarter 2013. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6. The inspectors reviewed the licensees reactor coolant system chemistry samples, technical specification requirements, issue reports, event reports, and NRC integrated inspection reports for the period of April 2012 through March 2013, to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. In addition to record reviews, the inspectors observed a chemistry technician obtain and analyze a reactor coolant system sample. Specific documents reviewed are described in the attachment to this report.

These activities constitute completion of two reactor coolant system specific activity samples as defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

.4 Reactor Coolant System Leakage (BI02)

a. Inspection Scope

The inspectors sampled licensee submittals for the reactor coolant system leakage performance indicator for both Units 1 and 2 for the period from the second quarter 2012 through the first quarter 2013. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6. The inspectors reviewed the licensees operator logs, reactor coolant system leakage tracking data, issue reports, event reports, and NRC integrated inspection reports for the period of April 2012 through March 2013 to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report.

These activities constitute completion of two reactor coolant system leakage samples as defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees corrective action program at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. The inspectors reviewed attributes that included the complete and accurate identification of the problem; the timely correction, commensurate with the safety significance; the evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and previous occurrences reviews; and the classification, prioritization, focus, and timeliness of corrective actions. Minor issues entered into the licensees corrective action program because of the inspectors observations are included in the attached list of documents reviewed.

These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure, they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report.

b. Findings

No findings were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensees corrective action program. The inspectors accomplished this through review of the stations daily corrective action documents.

The inspectors performed these daily reviews as part of their daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.

b. Findings

No findings were identified.

.3 Licensees Actions to Resolve Substantive Cross-Cutting Issue

a. Inspection Scope

The inspectors performed a review of the licensees corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors focused their review on substantive cross-cutting issue H.1(b), dealing with the licensees ability to use conservative decision making when evaluating and correcting problems (see Manual Chapter 0310, Components Within the Cross-Cutting Areas, Dated October 28, 2011, Section 06). The inspectors also discussed performance improvement details with licensee representatives, and performed a review of licensee initiatives to address deficiencies in the conservative decision making process. Documents reviewed by the inspectors are listed in an attachment to this report.

These activities constitute completion of one in-depth problem identification and resolution sample as defined in Inspection Procedure 71152-05.

b. Findings and Observations

No findings were identified. Overall, the licensees recovery plan appeared to address the appropriate deficiencies necessary for performance improvement.

4OA3 Followup of Events and Notices of Enforcement Discretion

(Closed) LER 05000368/2013-002-00, An Inoperable Emergency Control Room Chiller Due to Maintenance Error Results in a Prevented Safety Function.

On February 4, 2013, at 1255 CST, control room emergency chiller 2VE-1A breaker tripped shortly after the chiller was started. 2VE-1A is one of the two control room emergency chillers common to both Units 1 and 2. The licensee concluded that the cause of the breaker trip was that the C phase load side wire lug was not properly connected when the breaker was installed on November 15, 2012, resulting in a loose connection between the lug and the breaker stab. The condition was corrected and 2VE-1A was declared operable on February 6, 2013. The issue was entered into the corrective action program as Condition Report CR-ANO-2-2013-0233. The licensees corrective actions, as a result of the incorrectly installed breaker, included performing a human performance error review, including additional procedural requirements for visual verification of lug configuration for future breaker replacements, and reinspecting all previously replaced breakers identified in the extent of condition of the apparent cause evaluation. A Green self-revealing non-cited violation is documented below. This licensee event report is closed.

Failure to Correctly Install Control Room Emergency Chiller Supply Breaker

Introduction.

Inspectors documented a Green self-revealing non-cited violation of Technical Specification 6.4.1.a for the licensees failure to implement procedures recommended by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.

Specifically, the licensee failed to follow procedures for the replacement of the supply breaker for control room emergency chiller 2VE-1A. As a result, the breaker was installed incorrectly and the chiller was inoperable for over two months.

Description.

On February 4, 2013, the breaker for control room emergency chiller 2VE-1A tripped shortly after the chiller was started. When the electricians removed the molded case circuit breaker for testing they identified that the C phase load side wire lug was not properly installed in the breaker; the lug that tightens the wire down to the breaker stab was installed in front of the breaker stab instead of over it. This resulted in a loose connection between the lug and the breaker stab.

The licensee had installed the breaker in accordance with Procedure 1403.179, Molded Case Circuit Breaker Testing, Revision 20. Step 6.2.3 of Attachment 2 directed personnel to re-terminate the wires on the breaker. The location of this equipment made direct visual observation difficult necessitating the use of equipment, such as mirrors, to confirm proper installation. Although personnel installing the breaker were aware of the potential to incorrectly install the lug, they chose not to perform a visual verification of the connection, believing that if they pulled hard on the wires, and the wires did not pull out, it would confirm the lugs were installed properly. This assumption was incorrect because the wire could still be tightly pinched against the lug with the stab located outside of the lug. The licensee concluded that the causes of the incorrectly installed breaker were inadequate self-checks and peer-checks.

The breaker, which was installed on November 15, 2012, passed a monthly surveillance test directly after the post maintenance test and then again in December and January.

Even though the breaker passed three surveillance tests after its replacement, the licensee submitted a licensee event report because they concluded that the control room emergency chiller had not been operable because it had a loose electrical connection since November.

The licensee documented the issue in their corrective action program as CR-ANO-2-2013-00233. After repairs to the 2VE-1A breaker were made, including verification that the lug was correctly installed, a surveillance test was successfully completed on February 6, 2013. Other subsequent corrective actions included a human performance error review and additional procedural requirements for visual verification of the wire/lug connection for future breaker replacements. In addition, the licensee reinspected all previously replaced breakers identified in the apparent cause evaluation extent of condition.

Analysis.

Inspectors concluded that the failure to follow Procedure 1403.179 for replacement of the A train control room emergency chiller breaker is a performance deficiency. The performance deficiency is more than minor because it was associated

with the human performance attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences, and is therefore a finding. Specifically, the loose breaker connection adversely affected the availability and reliability of the control room emergency chiller A.

Using Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, and Appendix A, The Significance Determination Process (SDP) for Findings at Power, the inspectors determined that the finding required a detailed risk evaluation because it represented an actual loss of function of at least a single train for longer than its technical specification allowed outage time.

The senior reactor analyst performed a detailed risk evaluation using the Arkansas Nuclear One Standardized Plant Analysis Risk models Version 8.19 for Unit 1 and Version 8.21 for Unit 2, and various hand calculations. Additionally, the analyst used the seismic risk quantification method described in the Risk Assessment of Operational Events Handbook, Volume 2, External Events. The following calculations were performed:

  • Internal Initiators The analyst noted that the control room emergency chillers are only important to risk if the control room chilled water system is not available. The chilled water system is a fully functional backup to the emergency chillers provided they have electrical power. The chilled water system requires offsite power from either unit to function. Therefore, the dominant risk sequences for the control room emergency chillers will be upon loss of offsite power to both units.

The loss of offsite power frequency for either unit at Arkansas Nuclear One is 2.84 x 10-2/year as established in the SPAR model. The analyst used the conditional probabilities provided in Table 9 of the Idaho National Laboratories Loss of Offsite Power, 2011 Update, dated February 2013, to calculate the frequency of both units experiencing a loss of offsite power at the same time.

The combined frequency of a loss of offsite power affecting both units at Arkansas Nuclear One was 1.42 x 10-2/year.

The analyst reviewed Engineering Report 95-R-0013-01, Control Room Post Accident Ambient Temperature Requirements to determine the peak temperature limits for control room functionality. The limiting components were the high pressure injection flow instruments in Unit 2 which were designed to survive ambient control room temperatures of 122° F. As a bounding assumption, the analyst assumed that the operators and control room instrumentation could survive a peak of 120° F. From calculation CALC-10-E-0010-05, the analyst noted that Unit 2 heated up more rapidly than Unit 1 upon a postulated loss of cooling with 120° F being reached in 16.6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. Using the SPAR model, the analyst calculated a loss of offsite power nonrecovery probability for Unit 2 of

3.4 x 10-2. This resulted in an unrecovered frequency of losing the control room chilled water system of 4.8 x 10-4/year.

Using the SPAR model, the analyst estimated the failure probability of the control room emergency chillers (2.1 x 10-4) and Chiller 1B (2.4 x 10-2), assuming that Chiller 1A failed from the performance deficiency. Assuming that failure of all cooling for greater than 16.6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> would require a control room abandonment, the analyst set the conditional core damage probability to 0.1 as assumed in the Electric Power Research Institute, fire-induced vulnerability evaluation method.

The baseline conditional core damage frequency (CCDFBase) for this performance deficiency was calculated by multiplying the unrecovered frequency of losing the control room chilled water system (FNR-LOOP) with the failure probability of both trains of emergency chillers (Psys) and the conditional core damage probability of a main control room abandonment (CCDP) as follows:

CCDFBase = FNR-LOOP

  • Psys

= 4.8 x 10-4/year

  • 2.1 x 10-4
  • 0.1

= 1.0 x 10-8/year The finding conditional core damage frequency (CCDFCase) was calculated by assuming the failure probability of the chilled water system was now the failure probability of Chiller 1B (Ptrain) as follows:

CCDFCase = FNR-LOOP

  • Ptrain

= 4.8 x 10-4/year

  • 2.4 x 10-2
  • 0.1

= 1.2 x 10-6/year The analyst noted that the failure of Chiller 1A resulted from the improper termination of the associated breaker. The analyst assumed that the last time the breaker was successfully cycled resulted in the termination being incapable of providing sufficient current for the next start. The exposure period (EXP) was then determined to be the 25 days from the last successful test on January 10, 2013, until the observed failure on February 4, 2013, plus the 2 days it took to repair the condition and return the chiller to a functional status. Therefore, the incremental conditional core damage probability (ICCDP) for this performance deficiency was calculated as follows:

ICCDP = (CCDFCase - CCDFBase)

  • EXP / 365

= (1.2 x 10-6/year - 1.0 x 10-8/year)

  • 27 days / 365 days/year

= 8.4 x 10-8

  • Seismic Initiator The analyst used the plant-specific SPAR, Version 8.19 for Unit 1 and Version 8.21 for Unit 2 and a seismic model prepared as described in the Risk Assessment of Operational Events Handbook, Volume 2, External Events, to quantify the risk of this condition. To qualify the affect of the performance deficiency on the seismic risk, the analyst made the following assumptions:

o A seismic event that caused the failure of the ceramic insulators in the main switchyard would result in a loss of offsite power o A loss of offsite power caused by a seismic event would not be recoverable over the 24-hour response period assumed in this evaluation o Because differential movement is all that is necessary for failure of the improperly terminated power cable, the analyst assumed that the fragility of the termination was the same as the fragility of the ceramic insulators The analyst used 10 bins to characterize the peak ground acceleration during a postulated seismic event. In accordance with the Handbook rules, the frequency of a seismically induced loss of offsite power was calculated as 8.9 x 10-5/year.

In a similar manner, the frequency of a seismically-induced loss of offsite power with the failure of Control Room Emergency Chiller 1A was 3.8 x 10-5/year.

Using the method described under internal initiators, the analyst calculated a CCDFBase of 7.8 x 10-9/year and a CCDFCase of 9.0 x 10-7/year. Assuming that Chiller 1A was susceptible to failure during a seismic event for the 83 days from the installation of the breaker on November 15, 2012 until it was restored to a functional state on February 6, 2013, the ICCDP for seismic events was calculated to be 2.0 x 10-7.

In accordance with NRC Inspection Manual Chapter 0609, Appendix H, Table 5.1, Phase 1 Screening - Type A Findings at Full Power, none of the core damage sequences affected by this performance deficiency were important to the large, early release frequency. Therefore, based on the combined internal and seismic ICCDP of 2.9 x 10-7, this finding was of very low safety significance (Green).

The finding was determined to have a cross-cutting aspect in the area of human performance, associated with work practices, in that the licensee failed to use work practices that support human performance. Specifically, licensee personnel were aware

of the possibility of misaligning the wire grip style lug, but failed to use adequate self and peer checking to ensure the lug was correctly installed H.4(a).

Enforcement.

Technical Specification 6.4.1.a requires, in part, that written procedures be implemented covering the activities in Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978. Regulatory Guide 1.33, Appendix A, Section 9, specifies that procedures for performing maintenance that can affect the performance of safety-related equipment should be properly pre-planned and completed in accordance with written procedures and documented instructions appropriate to the circumstances.

Licensee Procedure 1403.179, Molded Case Circuit Breaker Testing, Revision 20, was a written procedure that implemented maintenance activities that can affect the performance of safety-related equipment. Procedure 1403.179, Attachment 2, Step 6.2.3 stated, in part, to re-terminate the wires on the breaker. Contrary to the above, the licensee failed to implement procedures covering maintenance activities that could affect the performance of safety-related equipment. Specifically, on November 15, 2012, the licensee failed to follow Procedure 1403.179 and properly re-terminate the wires on the train A control room emergency chiller supply breaker. After repairs to the 2VE-1A breaker were made, including verification that the lug was correctly installed, a surveillance test was successfully completed on February 6, 2013. Because this finding is of very low safety significance and has been entered into the corrective action program as Condition Report CR-ANO-2-2013-00233, this violation is being treated as a non-cited violation consistent with Section 2.3.2.a of the NRC Enforcement Policy:

NCV 05000368/2013003-02, Failure to Correctly Install Control Room Emergency Chiller Supply Breaker.

4OA5 Other Activities

.1 (Discussed) NRC Temporary Instruction 2515/182, Review of the Implementation of the

Industry Initiative to Control Degradation of Underground Piping and Tanks Leakage from buried and underground pipes has resulted in ground water contamination incidents with associated heightened NRC and public interest. The industry issued a guidance document, Nuclear Energy Institute 09-14, Guideline for the Management of Buried Piping Integrity (ADAMS Accession No. ML1030901420) to describe the goals and commitments made by the licensee resulting from this underground piping and tank initiative. On December 31, 2010, the Nuclear Energy Institute issued Revision 1 to Nuclear Energy Institute 09-14 (ADAMS Accession No. ML110700122) with an expanded scope of components which included underground piping that was not in direct contact with the soil and underground tanks. On November 17, 2011, the NRC issued Temporary Instruction 2515/182, Review of the Industry Initiative to Control Degradation of Underground Piping and Tanks, to gather information related to the industrys implementation of this initiative.

a. Inspection Scope

The inspectors reviewed the licensees programs for buried pipe, underground piping, and tanks in accordance with Temporary Instruction 2515/182 to determine if the program attributes and completion dates identified in Sections 3.3 A and 3.3 B of

Nuclear Energy Institute 09-14, Revision 1, were contained in the licensees program and implementing procedures. For the buried pipe and underground piping program attributes with completion dates that had passed, the inspectors reviewed records to determine if the attribute was in fact complete.

b. Findings

No findings were identified.

.2 (Closed) Temporary Instruction 2515/187, Inspection of Near-Term Task Force

Recommendation 2.3 Flooding Walkdowns

a. Inspection Scope

Inspectors verified that licensees walkdown packages for the Units 1 and 2 intake structures contained the elements as specified in Nuclear Energy Institute 12-07 Walkdown Guidance.

The inspectors independently performed a walkdown of the Units 1 and 2 intake structures. The inspectors confirmed that the licensee verified the following flood protection features:

  • External visual inspection for indications of degradation that would prevent its credited function from being performed was performed
  • Critical structure, system, and component dimensions were measured
  • Available physical margin, where applicable, was determined
  • Flood protection feature functionality was determined using either visual observation or by review of other documents The inspectors verified that non-compliances with current licensing requirements, and issues identified in accordance with the 10 CFR 50.54(f) letter, Item 2.g of Enclosure 4, were entered into the licensee's corrective action program. In addition, issues identified in response to Item 2.g that could challenge risk significant equipment and the licensees ability to mitigate the consequences will be subject to additional NRC evaluation.

b. Findings

No findings identified.

.3 (Closed) Temporary Instruction 2515/188, Inspection of Near-Term Task Force

Recommendation 2.3 Seismic Walkdowns

a. Inspection Scope

The inspector independently performed a seismic walkdown of Unit 2 2CV-1052, steam generator B atmospheric dump control valve.

Additionally, inspectors verified that items that could allow the spent fuel pool to drain down rapidly were walked down by the licensee.

The inspectors independently verified that the following seismic features were free of potential adverse seismic conditions:

  • Anchorage was free of bent, broken, missing or loose hardware
  • Anchorage was free of corrosion that was more than mild surface oxidation
  • Anchorage was free of visible cracks in the concrete near the anchors
  • Anchorage configuration was consistent with plant documentation
  • SSCs would not be damaged from impact by nearby equipment or structures
  • Overhead equipment, distribution systems, ceiling tiles and lighting, and masonry block walls were secure and not likely to collapse onto the equipment
  • Attached lines had adequate flexibility to avoid damage
  • The area appeared to be free of potentially adverse seismic interactions that could cause flooding or spray in the area
  • The area appeared to be free of potentially adverse seismic interactions that could cause a fire in the area
  • The area appeared to be free of potentially adverse seismic interactions associated with housekeeping practices, storage of portable equipment, and temporary installations (e.g., scaffolding, lead shielding)

Observations made during the walkdown that could not be determined to be acceptable were entered into the licensees corrective action program for evaluation.

b. Findings

No findings identified.

4OA6 Meetings, Including Exit

Exit Meeting Summary

On May 16, 2013, the inspectors presented the inspection results of the review of inservice inspection activities to Mr. D. James, Nuclear Safety Assurance Director, and other members of the licensee staff. The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.

On July 2, 2013, the inspectors presented the inspection results to Mr. J. Browning, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

A. Remer, Project Manager
B. Greeson, Engineering, Procurement Manager
D. Hughes, Engineering Supervisor
D. James, Nuclear Safety Assurance Director
D. Meatheany, Steam Generator Lead
D. Perkins, Maintenance Manager
J. Browning, Site Vice President
J. Gobell, Welding Engineer
J. Tobin, Security Manager
K. Panther, Nondestructive Examination Lead
M. Chisum, General Manager Plant Operations
M. Hall, Licensing Specialist
N. Mosher, Licensing Specialist
P. Schlutermor, Boric Acid Lead
R. Fuller, Nuclear Oversight Manager
S. Pyle, Licensing Manager

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000368/2013003-01 NCV Failure to Evaluate and Correct Excessive Containment Isolation Valve Leakage (Section 1R22)
05000368/2013003-02 NCV Failure to Correctly Install Control Room Emergency Chiller Supply Breaker (Section 40A3)

Closed

An Inoperable Emergency Control Room Chiller Due to

05000368/2013-002-00 LER Maintenance Error Results in a Prevented Safety Function (Section 4OA3)

Inspection of Near-Term Task Force Recommendation 2.3 2515/187 TI Flooding Walkdowns (Section 4OA5.2)

Attachment 1

Inspection of Near-Term Task Force Recommendation 2.3 2515/188 TI Seismic Walkdowns (Section 4OA5.3)

Discussed

Review of the Implementation of the Industry Initiative to Control 2515/182 TI Degredation of Underground Piping and Tanks (Section 4OA5.1)

LIST OF DOCUMENTS REVIEWED