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| issue date = 05/08/2015 | | issue date = 05/08/2015 | ||
| title = IR 05000338/2015-001, 05000339/2015-001; 01/01/2015 - 03/31/2015; North Anna Power Station, Units 1 and 2. Maintenance Effectiveness | | title = IR 05000338/2015-001, 05000339/2015-001; 01/01/2015 - 03/31/2015; North Anna Power Station, Units 1 and 2. Maintenance Effectiveness | ||
| author name = Rose S | | author name = Rose S | ||
| author affiliation = NRC/RGN-II/DRP/RPB5 | | author affiliation = NRC/RGN-II/DRP/RPB5 | ||
| addressee name = Heacock D | | addressee name = Heacock D | ||
| addressee affiliation = Virginia Electric & Power Co (VEPCO) | | addressee affiliation = Virginia Electric & Power Co (VEPCO) | ||
| docket = 05000338, 05000339 | | docket = 05000338, 05000339 | ||
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=Text= | =Text= | ||
{{#Wiki_filter:UNITED STATES | {{#Wiki_filter:UNITED STATES May 8, 2015 | ||
==SUBJECT:== | |||
NORTH ANNA POWER STATION - NRC INTEGRATED INSPECTION REPORT 05000338/2015001 and 05000339/2015001 | |||
SUBJECT: NORTH ANNA POWER STATION - NRC INTEGRATED INSPECTION REPORT 05000338/2015001 and 05000339/2015001 | |||
==Dear Mr. Heacock:== | ==Dear Mr. Heacock:== | ||
On March 31, 2015, the U. S. Nuclear Regulatory Commission (NRC) completed an inspection at your North Anna Power Station, Units 1 and 2. On April 22 , 2015, the NRC inspectors discussed the results of this inspection with Mr. G. Bischof and other members of your staff | On March 31, 2015, the U. S. Nuclear Regulatory Commission (NRC) completed an inspection at your North Anna Power Station, Units 1 and 2. On April 22, 2015, the NRC inspectors discussed the results of this inspection with Mr. G. Bischof and other members of your staff. | ||
Inspectors documented the results of this inspection in the enclosed inspection report. | |||
safety significance (Green) in this report which was determined to involve a violation of NRC requirements. The NRC is treating this finding as a non-cited violation (NCV) consistent with Section 2.3.2 of the NRC Enforcement Policy. | Nuclear Regulatory Commission inspectors documented one self-revealing finding of very low safety significance (Green) in this report which was determined to involve a violation of NRC requirements. The NRC is treating this finding as a non-cited violation (NCV) consistent with Section 2.3.2 of the NRC Enforcement Policy. | ||
If you wish to contest this NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: | If you wish to contest this NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: | ||
Document Control Desk, Washington, DC 20555-001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the North Anna Power | Document Control Desk, Washington, DC 20555-001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the North Anna Power Station. | ||
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the North Anna Power Station. In accordance with Title 10 Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding, of the NRC's "Agency Rules of Practice and Procedure," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS) component of NRC's Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | |||
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the North Anna Power | |||
Station. In accordance with Title 10 Code of Federal Regulations 2.390, | |||
Sincerely, | Sincerely, | ||
/RA/ Steven D. Rose, Chief Reactor Projects Branch 5 Division of Reactor Projects | /RA/ | ||
Steven D. Rose, Chief Reactor Projects Branch 5 Division of Reactor Projects Docket Nos.: 05000338, 05000339 License Nos.: NPF-4, NPF-7 | |||
===Enclosure:=== | |||
IR 05000338/2015001 and 05000339/2015001 w/ Attachment: Supplementary Information | |||
License Nos | REGION II== | ||
Docket Nos: 50-338, 50-339 License Nos: NPF-4, NPF-7 Report No: 05000338/2015001 and 05000339/2015001 Licensee: Virginia Electric and Power Company (VEPCO) | |||
Facility: North Anna Power Station, Units 1 & 2 Location: Mineral, Virginia 23117 Dates: January 1, 2015 through March 31, 2015 Inspectors: G.Kolcum, Senior Resident Inspector G. Skaggs Ryan, Resident Inspector R. Carrion, Senior Reactor Engineer, Section 1R08 R. Hamilton, Senior Health Physicist, Section 2RS1 Approved by: Steven D. Rose, Chief Reactor Projects Branch 5 Division of Reactor Projects Enclosure | |||
=SUMMARY= | |||
IR 05000338/2015-001, 05000339/2015-001; 01/01/2015 - 03/31/2015; North Anna Power | |||
Station, Units 1 and 2. Maintenance Effectiveness. | |||
The report covered a three-month period of inspection by resident inspectors and senior operations engineers from the region | The report covered a three-month period of inspection by resident inspectors and senior operations engineers from the region. One self-revealing finding was identified and was determined to be a non-cited violation (NCV). The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, | ||
. One self-revealing finding was identified and was determined to be a non-cited violation (NCV). The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, | Significance Determination Process (SDP). The cross-cutting aspect was determined using IMC 0310, Components Within the Cross Cutting Areas. All violations of NRC requirements are dispositioned in accordance with the NRCs Enforcement Policy, dated February 5, 2015. | ||
The | The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 5, dated February 2014. | ||
===Cornerstone: Barrier Integrity=== | ===Cornerstone: Barrier Integrity=== | ||
: '''Green.''' | : '''Green.''' | ||
A self-revealing NCV of 10 CFR 50 Appendix B, Criterion V, | A self-revealing NCV of 10 CFR 50 Appendix B, Criterion V, Instructions, | ||
Procedures, and Drawings, was identified for the licensees failure to follow work management procedures. Specifically, the licensee failed to follow the conduct of maintenance procedure, MM-AA-100, Conduct of Maintenance, Revision 10, where maintenance personnel should use an assortment of techniques and tools to avoid errors during work execution. Attachment 6 step 1b outlines various human error prevention techniques that should have been used during the work execution including self checking and questioning attitude. This issue was entered this into the licensees corrective action program as CR 567185. | |||
The | The licensees failure to follow the conduct of maintenance procedure, MM-AA-100, | ||
Conduct of Maintenance, Revision 10, was a performance deficiency. Specifically, on December 10, 2014, maintenance personnel failed to effectively use human error prevention tools when performing the maintenance on the Refueling Water Storage Tank (RWST) level channels which resulted in a loss of the safety function of the Recirculation Spray (RS)system. The performance deficiency was more than minor because it was associated with the configuration control attribute of the Barrier Integrity cornerstone and adversely affected the cornerstone objective to ensure that the physical design barriers (fuel cladding, reactor coolant system, and containment) protect the public from radionuclide releases caused by accidents or events and is therefore a finding. Specifically, the RS system safety function was inadvertently rendered inoperable. The inspectors performed a Phase 1 analysis using the IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 3 Barrier Integrity Screening Questions, dated June 19, 2012 and Appendix H, Containment Integrity Significance Determination Process, dated May 6, 2004, and determined the finding required a detailed risk evaluation because it involved the loss of safety function of the RS system. | |||
A detailed risk evaluation was performed in accordance with NRC Inspection Manual Chapter (IMC) 0609, Appendix A by a regional | A detailed risk evaluation was performed in accordance with NRC Inspection Manual Chapter (IMC) 0609, Appendix A by a regional senior reactor analyst using the latest NRC North Anna SPAR model and Saphire risk program. The major analysis assumptions included: a thirty-two minute exposure interval, and a non-recoverable loss of both inside recirculation spray pumps and both outside recirculation pumps. The dominant risk sequence was a small break loss of coolant accident initiator, success of the reactor protection system, success of feedwater, success of high pressure injection, success of secondary side cooldown and failure of recirculation spray resulting in loss of core and containment heat removal capability. The risk was mitigated by the short exposure period. | ||
The risk evaluation result was an increase in core damage frequency of <1 E-6/year and an increase in large early release fraction of <1 E -7/year, a GREEN finding of very low safety significance. | The risk evaluation result was an increase in core damage frequency of <1 E-6/year and an increase in large early release fraction of <1 E -7/year, a GREEN finding of very low safety significance. | ||
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===Summary of Plant Status=== | ===Summary of Plant Status=== | ||
Unit 1 entered a forced outage due to a leak in a Reactor Coolant System (RCS) drain pipe on December 22, 2014. Unit 1 began the period at full Rated Thermal Power (RTP) and operated at full power until the Unit experienced an automatic trip on February 26, 2015, due to a circuit card failure on | Unit 1 entered a forced outage due to a leak in a Reactor Coolant System (RCS) drain pipe on December 22, 2014. Unit 1 began the period at full Rated Thermal Power (RTP) and operated at full power until the Unit experienced an automatic trip on February 26, 2015, due to a circuit card failure on B main feed regulating valve for B steam generator level control. Unit 1 restarted on February 28, 2015, and returned to ninety percent power on March 2, 2015. Unit 1 went off line on March 7, 2015, for the planned spring refueling outage. Unit 1 started up on March 28 and returned online March 29, 2015, and returned to full RTP on March 30, 2015. | ||
Unit 2 began the period at full RTP and operated at full power for the entire report period. | Unit 2 began the period at full RTP and operated at full power for the entire report period. | ||
==REACTOR SAFETY== | ==REACTOR SAFETY== | ||
Cornerstones: | Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity | ||
{{a|1R01}} | |||
{{a|1R01}} | |||
==1R01 Adverse Weather Protection== | ==1R01 Adverse Weather Protection== | ||
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====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed the | The inspectors reviewed the licensees adverse weather preparations for cold weather operations specified in 0-GOP-4, Cold Weather Operations, Revision 56, 0-GOP-4.2, Extreme Cold Weather Operations, Revision 36, and 0-GOP-4.2A, Extreme Cold Weather Daily Checks, Revision 8, as well as the licensees corrective action data base for cold weather related issues. The inspectors walked down the risk-significant areas listed below on two occasions to verify compliance with procedural requirements and to verify that the specified actions provided the necessary protection for the applicable structures, systems, or components (SSCs). The inspectors reviewed the licensees corrective action program (CAP) database to verify that weather related problems due to temperature were being identified at the appropriate level, entered into the CAP, and appropriately resolved. | ||
, as well as the | |||
* Unit 1 and 2 Emergency Diesel Generator Rooms and Station Blackout (SBO) Diesel on January 7, 2015 with weather in the teens | * Unit 1 and 2 Emergency Diesel Generator Rooms and Station Blackout (SBO) Diesel on January 7, 2015 with weather in the teens | ||
* Unit 1 and 1 Emergency Diesel Generator room and the SBO Emergency Diesel Generator on February 15, 2015 with temperatures below 15 degrees Fahrenheit | * Unit 1 and 1 Emergency Diesel Generator room and the SBO Emergency Diesel Generator on February 15, 2015 with temperatures below 15 degrees Fahrenheit | ||
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====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors performed a site specific weather related inspection due to anticipated adverse weather conditions. On February 2, 2015, the inspectors reviewed the licensee response to high wind warnings of 25 to 35 miles an hour with gusts up to 40 miles an hour for the area. Specifically, the inspectors reviewed licensee adverse weather response procedures, including 0-AP-41, | The inspectors performed a site specific weather related inspection due to anticipated adverse weather conditions. On February 2, 2015, the inspectors reviewed the licensee response to high wind warnings of 25 to 35 miles an hour with gusts up to 40 miles an hour for the area. Specifically, the inspectors reviewed licensee adverse weather response procedures, including 0-AP-41, Severe Weather Conditions, Revision 61, and site preparations including work activities that could impact the overall maintenance risk assessments. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R04}} | ||
{{a|1R04}} | |||
==1R04 Equipment Alignment== | ==1R04 Equipment Alignment== | ||
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====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors conducted seven equipment alignment partial walkdowns, listed below, to evaluate the operability of selected redundant trains or backup systems with the other train or system inoperable or out of service. The inspectors reviewed the functional systems descriptions, Updated Final Safety Analysis Report (UFSAR), system operating procedures, and Technical Specifications (TS) to determine correct system lineups for the current plant conditions. The inspectors performed walkdowns of the systems to verify the operability of a redundant or backup system/train or a remaining operable system/train with a high risk significance for the current plant configuration (considering out-of-service, inoperable, or degraded condition); or a risk-significant system/train that was recently realigned following an extended | The inspectors conducted seven equipment alignment partial walkdowns, listed below, to evaluate the operability of selected redundant trains or backup systems with the other train or system inoperable or out of service. The inspectors reviewed the functional systems descriptions, Updated Final Safety Analysis Report (UFSAR), system operating procedures, and Technical Specifications (TS) to determine correct system lineups for the current plant conditions. The inspectors performed walkdowns of the systems to verify the operability of a redundant or backup system/train or a remaining operable system/train with a high risk significance for the current plant configuration (considering out-of-service, inoperable, or degraded condition); or a risk-significant system/train that was recently realigned following an extended system outage, maintenance, modification, or testing; or a risk-significant single-train system. The inspector conducted the reviews to ensure that critical components were properly aligned, and to identify any discrepancies which could affect operability of the redundant train or backup system. | ||
* Unit 1 Auxiliary Feedwater (AFW) Terry Turbine during startup preparations after refueling | * Unit 1 Auxiliary Feedwater (AFW) Terry Turbine during startup preparations after refueling | ||
* Unit 1 Motor-Driven AFW trains | * Unit 1 Motor-Driven AFW trains A and B during startup preparations after refueling | ||
* 1H and 1J Emergency Diesel Generators (EDGs) during startup preparations after refueling | * 1H and 1J Emergency Diesel Generators (EDGs) during startup preparations after refueling | ||
* Unit 1 component cooling heat exchangers after maintenance on | * Unit 1 component cooling heat exchangers after maintenance on A component cooling heat exchanger | ||
* 1H EDG fuel oil transfer system | * 1H EDG fuel oil transfer system | ||
* Unit 1 charging pumps during maintenance on | * Unit 1 charging pumps during maintenance on B charging pump | ||
* Unit 2 | * Unit 2 B low head safety injection pump | ||
====b. Findings==== | ====b. Findings==== | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R05}} | ||
{{a|1R05}} | |||
==1R05 Fire Protection== | ==1R05 Fire Protection== | ||
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====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors conducted focused tours of the five areas listed below that are important to reactor safety to verify the | The inspectors conducted focused tours of the five areas listed below that are important to reactor safety to verify the licensees implementation of fire protection requirements as described in fleet procedures CM-AA-FPA-100, Fire Protection/Appendix R (Fire Safe Shutdown) Program, Revision 10, CM-AA-FPA-101, Control of Combustible and Flammable Materials, Revision 6, and CM-AA-FPA-102, Fire Protection and Fire Safe Shutdown Review and Preparation Process and Design Change Process, Revision 5. | ||
Revision 10, CM-AA-FPA-101, | |||
The inspectors evaluated, as appropriate, conditions related to: | The inspectors evaluated, as appropriate, conditions related to: | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R06}} | ||
{{a|1R06}} | |||
==1R06 Flood Protection Measures== | ==1R06 Flood Protection Measures== | ||
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====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors assessed the internal flooding vulnerability of the two flood areas listed below with respect to adjacent safety-related areas to verify that the flood protection barriers and equipment were being maintained consistent with the UFSAR. The | The inspectors assessed the internal flooding vulnerability of the two flood areas listed below with respect to adjacent safety-related areas to verify that the flood protection barriers and equipment were being maintained consistent with the UFSAR. The licensees corrective action documents were reviewed to verify that corrective actions with respect to flood-related items identified in condition reports were adequately addressed. The inspectors conducted a field survey of the selected areas to evaluate the adequacy of flood barriers, and floor drains to protect the equipment, as well as their overall material condition. | ||
* Unit 1 AFW Pump House | * Unit 1 AFW Pump House | ||
* Fuel Oil Pump House | * Fuel Oil Pump House | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R07}} | ||
{{a|1R07}} | |||
==1R07 Heat Sink Performance== | ==1R07 Heat Sink Performance== | ||
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====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors selected the risk significant Unit 1 | The inspectors selected the risk significant Unit 1 B Charging Pump Lube Oil Heat Exchangers (HXs) for the 1B Gear Box Lube Oil Cooler and reviewed inspection records, test results, maintenance work orders, and other documentation to ensure that deficiencies which could mask or degrade performance were identified and corrected. | ||
The test procedures and records were also reviewed to verify that they were consistent with Generic Letter 89-13 licensee commitments, and Electric Power Research Institute (EPRI) Heat Exchanger Performance Monitoring Guidelines. In addition, the inspectors reviewed inspection documentation of the related service water piping to assess general material condition and to identify any degraded conditions. Documents reviewed included Virginia Power Administrative Procedure (VPAP) -0811, | The test procedures and records were also reviewed to verify that they were consistent with Generic Letter 89-13 licensee commitments, and Electric Power Research Institute (EPRI) Heat Exchanger Performance Monitoring Guidelines. In addition, the inspectors reviewed inspection documentation of the related service water piping to assess general material condition and to identify any degraded conditions. Documents reviewed included Virginia Power Administrative Procedure (VPAP) -0811, Service Water Inspection and Maintenance Program, Revision 6, and licensee procedure ER-AA-HTX-1003, Heat Exchanger Monitoring and Assessment, Revision 6. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R08}} | ||
{{a|1R08}} | |||
==1R08 Inservice Inspection Activities== | ==1R08 Inservice Inspection Activities== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
Non-Destructive Examination Activities and Welding Activities From March 19 - 23, 2015, the inspectors conducted an onsite review of the implementation of the | Non-Destructive Examination Activities and Welding Activities From March 19 - 23, 2015, the inspectors conducted an onsite review of the implementation of the licensees inservice inspection (ISI) program for monitoring degradation of the reactor coolant system boundary, risk-significant piping and component boundaries, and containment boundaries in Unit 1. | ||
The inspectors either directly observed or reviewed the following non-destructive examinations (NDEs) mandated by the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (Code of Record: | The inspectors either directly observed or reviewed the following non-destructive examinations (NDEs) mandated by the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (Code of Record: 2004 Edition with 2006 Addenda) to evaluate compliance with the ASME Code, Section XI and Section V requirements, and if any indications or defects were detected, to evaluate if they were dispositioned in accordance with the ASME Code or an NRC-approved alternative requirement. (Note: The Code of Record for IWE and IWL is the 2001 Edition with 2003 Addenda.) The inspectors also reviewed the qualifications of the NDE technicians performing the examinations, to determine whether they were current and in compliance with the ASME Code requirements. | ||
* Ultrasonic Testing (UT), Weld 11715-WMKS-0102C/16-WFPD-22/18A, Elbow to Nozzle Weld, Class 2 (observed) | * Ultrasonic Testing (UT), Weld 11715-WMKS-0102C/16-WFPD-22/18A, Elbow to Nozzle Weld, Class 2 (observed) | ||
* Magnetic Particle Testing (MT), Weld 11715-WMKS-RC-E2/1-RC-E-2/8, Pressurizer Integral Attachment (reviewed) | * Magnetic Particle Testing (MT), Weld 11715-WMKS-RC-E2/1-RC-E-2/8, Pressurizer Integral Attachment (reviewed) | ||
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* Visual Testing (VT)-15-024, Restraint 11715-WMKS-0103AT/2-CH-96/R24 (reviewed) | * Visual Testing (VT)-15-024, Restraint 11715-WMKS-0103AT/2-CH-96/R24 (reviewed) | ||
* VT-15-032, Restraint 11715-WMKS-01031B/32-SHP-1/R44 (reviewed) | * VT-15-032, Restraint 11715-WMKS-01031B/32-SHP-1/R44 (reviewed) | ||
* Phased array UT, Weld 11715-WMKS-RC-E-1A.2/29-RC-1/N-SE29IN, | * Phased array UT, Weld 11715-WMKS-RC-E-1A.2/29-RC-1/N-SE29IN, A SG Hot Leg WOR (Weld Overlay Repair) (reviewed) | ||
* Phased array UT, Weld 11715-WMKS-RC-E-1B.2/29-RC-4/N-SE29IN, | * Phased array UT, Weld 11715-WMKS-RC-E-1B.2/29-RC-4/N-SE29IN, B SG Hot Leg WOR (reviewed) | ||
* Phased array UT, Weld N-SE31 IN, | * Phased array UT, Weld N-SE31 IN, B SG Cold Leg DM Weld (reviewed) | ||
* Phased array UT, Weld N-SE31 IN, | * Phased array UT, Weld N-SE31 IN, C SG Cold Leg DM Weld (reviewed) | ||
The inspectors reviewed the following welding activities to evaluate compliance with procedures, and the ASME Code Section XI and Section IX requirements. Specifically, the inspectors reviewed the associated work orders, repair and replacement plans, weld data sheets, welding procedures, procedure qualification records, welder performance qualification records, and NDE reports. | The inspectors reviewed the following welding activities to evaluate compliance with procedures, and the ASME Code Section XI and Section IX requirements. Specifically, the inspectors reviewed the associated work orders, repair and replacement plans, weld data sheets, welding procedures, procedure qualification records, welder performance qualification records, and NDE reports. | ||
* Replacement of 3" Velan Check Valve, Class 1 (reviewed) | * Replacement of 3" Velan Check Valve, Class 1 (reviewed) | ||
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* Valve Replacement of 1-CH-302, 4B Seal Water Injection Filter Inlet Isolation Valve (reviewed) | * Valve Replacement of 1-CH-302, 4B Seal Water Injection Filter Inlet Isolation Valve (reviewed) | ||
* Permanent Shielding for Charging Letdown Piping (reviewed) | * Permanent Shielding for Charging Letdown Piping (reviewed) | ||
* Replacement of 2 | * Replacement of 2 Elbow on C Loop Drain Line. (reviewed) | ||
During non-destructive surface and volumetric examinations performed since the previous refueling outage, the licensee did not identify any relevant indications that were analytically evaluated and accepted for continued service; therefore, no NRC review was completed for this inspection procedure attribute. | During non-destructive surface and volumetric examinations performed since the previous refueling outage, the licensee did not identify any relevant indications that were analytically evaluated and accepted for continued service; therefore, no NRC review was completed for this inspection procedure attribute. | ||
Pressurized Water Reactor Vessel Upper Head Penetration Inspection Activities The inspectors verified that for the Unit 1 vessel head, a bare metal visual (BMV) examination and a volumetric examination were not required during this outage, in accordance with the requirements of ASME Code Case N-729-1 and 10 CFR 50.55a(g)(6)(ii)(D). The inspectors also reviewed the | Pressurized Water Reactor Vessel Upper Head Penetration Inspection Activities The inspectors verified that for the Unit 1 vessel head, a bare metal visual (BMV)examination and a volumetric examination were not required during this outage, in accordance with the requirements of ASME Code Case N-729-1 and 10 CFR 50.55a(g)(6)(ii)(D). The inspectors also reviewed the licensees Alloy 600 Management Plan, to verify the implemented strategy provides reasonable assurance that plant safety will be maintained. | ||
The licensee did not identify any relevant indications that were accepted for continued service during the previous BMV exams. Additionally, the licensee did not perform any welding repairs to the vessel head penetrations since the beginning of the last Unit 1 refueling outage; therefore, no NRC review was completed for these inspection procedure attributes. | |||
Boric Acid Corrosion Control Inspection Activities The inspectors reviewed the licensees boric acid corrosion control program (BACCP)activities to ensure implementation with commitments made in response to NRC Generic Letter 88-05, Boric Acid Corrosion of Carbon Steel Reactor Pressure Boundary Components in PWR Plants, and applicable industry guidance documents. Specifically, the inspectors performed an onsite record review of procedures, and the results of the licensees containment walkdown inspections performed during the current spring refueling outage. The inspectors also interviewed the BACCP owner, conducted an independent walkdown of containment to evaluate compliance with licensees BACCP requirements, and verified that degraded or non-conforming conditions, such as boric acid leaks, were properly identified and corrected in accordance with the licensees BACCP, and corrective action program (CAP). The inspectors also reviewed the BACCP health reports since the last Unit 1 outage to evaluate program trends. | |||
Boric Acid Corrosion Control Inspection Activities | |||
The inspectors reviewed the | |||
The inspectors reviewed the following engineering evaluations completed for evidence of boric acid leakage, to determine if the licensee properly applied applicable corrosion rates to the affected components; and properly assessed the effects of corrosion induced wastage on structural or pressure boundary integrity in accordance with the licensee procedures. | The inspectors reviewed the following engineering evaluations completed for evidence of boric acid leakage, to determine if the licensee properly applied applicable corrosion rates to the affected components; and properly assessed the effects of corrosion induced wastage on structural or pressure boundary integrity in accordance with the licensee procedures. | ||
* Inservice Inspection Indication Evaluation Record for Code Case N-566-2 Compliance, Initiating Condition Report: | * Inservice Inspection Indication Evaluation Record for Code Case N-566-2 Compliance, Initiating Condition Report: 573530 | ||
* Inservice Inspection Indication Evaluation Record for Code Case N-566-2 Compliance, Initiating Condition Report: | * Inservice Inspection Indication Evaluation Record for Code Case N-566-2 Compliance, Initiating Condition Report: 573571 The inspectors reviewed the following condition reports (CRs) and associated corrective actions related to evidence of boric acid leakage, to evaluate if the corrective actions completed were consistent with the requirements of the ASME Code and 10 CFR Part 50, Appendix B, Criterion XVI. | ||
CR 568076, Boric Acid Discovered at 1-IC-26 CR 568077, Boric Acid Discovered at 1-IC-1 CR 568078, Boric Acid Discovered at 1-IC-4 CR 568080, Boric Acid Discovered at 1-RC-1053 CR 568082, Boric Acid Discovered at 1-RC-1057 CR 568083, Boric Acid Discovered at Union Associated with 1-RC-RV-1 CR 568084, Boric Acid Discovered at 1-CH-332 CR 568107, Boric Acid Leakage Discovered at 1-SS-TV-109B CR 568109, Boric Acid Leakage Discovered at 1-RC-69 CR 568119, Boric Acid Leakage Discovered at 1-CH-360 CR 568121, Boric Acid Leakage Discovered at Various Components CR 568125, Boric Acid Leakage Discovered at Various Components Identification and Resolution of Problems The inspectors reviewed a sample of ISI-related issues entered into the CAP to determine if the licensee had appropriately described the scope of the problem, and had initiated corrective actions. The review also included the licensees consideration and assessment of operating experience events applicable to the plant. The inspectors performed this review to ensure compliance with 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requirements. | |||
CR 568076, Boric Acid Discovered at 1-IC-26 CR 568077, Boric Acid Discovered at 1-IC-1 CR 568078, Boric Acid Discovered at 1-IC-4 CR 568080, Boric Acid Discovered at 1-RC-1053 CR 568082, Boric Acid Discovered at 1-RC-1057 CR 568083, Boric Acid Discovered at Union Associated with 1-RC-RV-1 CR 568084, Boric Acid Discovered at 1-CH-332 CR 568107, Boric Acid Leakage Discovered at 1-SS-TV-109B CR 568109, Boric Acid Leakage Discovered at 1-RC-69 CR 568119, Boric Acid Leakage Discovered at 1-CH-360 CR 568121, Boric Acid Leakage Discovered at Various Components CR 568125, Boric Acid Leakage Discovered at Various Components | |||
Identification and Resolution of Problems The inspectors reviewed a sample of ISI-related issues entered into the CAP to determine if the licensee had appropriately described the scope of the problem, and had initiated corrective actions. The review also included the | |||
XVI, | |||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R11}} | ||
{{a|1R11}} | |||
==1R11 Licensed Operator Requalification Program and Licensed Operator Performance== | ==1R11 Licensed Operator Requalification Program and Licensed Operator Performance== | ||
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====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed a licensed operator performance on January 14, 2015, during a | The inspectors reviewed a licensed operator performance on January 14, 2015, during a simulator scenario which involved a steam generator tube rupture and an emergency boration for a reactor failing to trip. The scenario required classifications and notifications that were counted for NRC performance indicator input. | ||
simulator scenario which involved a steam generator tube rupture and an emergency boration for a reactor failing to trip. The scenario required classifications and notifications that were counted for NRC performance indicator input. | |||
The inspectors observed the following | The inspectors observed the following elements of crew performance in terms of communications: | ||
: (1) ability to take timely and proper actions; | : (1) ability to take timely and proper actions; | ||
: (2) prioritizing, interpreting, and verifying alarms; | : (2) prioritizing, interpreting, and verifying alarms; | ||
: (3) correct use and implementation of procedures, including the alarm response procedures; | : (3) correct use and implementation of procedures, including the alarm response procedures; | ||
: (4) timely control board operation and manipulation, including high-risk operator actions; and, | : (4) timely control board operation and manipulation, including high-risk operator actions; and, | ||
: (5) oversight and direction provided by the shift supervisor, including the ability to identify and implement appropriate TS actions. The inspectors observed the post training critique to determine that weaknesses or improvement areas revealed by the training were captured by the instructor and reviewed with the operators. Documents reviewed are listed in the Attachment to this | : (5) oversight and direction provided by the shift supervisor, including the ability to identify and implement appropriate TS actions. The inspectors observed the post training critique to determine that weaknesses or improvement areas revealed by the training were captured by the instructor and reviewed with the operators. Documents reviewed are listed in the Attachment to this report. | ||
report. | |||
====b. Findings==== | ====b. Findings==== | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R12}} | ||
{{a|1R12}} | |||
==1R12 Maintenance Effectiveness== | ==1R12 Maintenance Effectiveness== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
For the three equipment issues listed below, the inspectors evaluated the effectiveness of the respective licensee's preventive and corrective maintenance. The inspectors performed walkdowns of the accessible portions of the systems, performed in-office reviews of procedures and evaluations, and held discussions with licensee staff. The inspectors compared the | For the three equipment issues listed below, the inspectors evaluated the effectiveness of the respective licensee's preventive and corrective maintenance. The inspectors performed walkdowns of the accessible portions of the systems, performed in-office reviews of procedures and evaluations, and held discussions with licensee staff. The inspectors compared the licensees actions with the requirements of the Maintenance Rule (10 CFR 50.65), and licensee procedure ER-AA-MRL-10, Maintenance Rule Program, Revision 6. Other documents reviewed are listed in the Attachment to this report. | ||
* CR568982, | * CR568982, Drive gear broken on 1-SW-230 | ||
* CR568951, | * CR568951, Hydro Test Pump speed control constant at varying outputs | ||
* CR567185, | * CR567185, Two channels of U1 RWST level removed from service during calibrations | ||
====b. Findings==== | ====b. Findings==== | ||
avoid errors during work execution. Attachment 6 step 1b outlines various human error prevention techniques that should have been used during the work execution including | =====Introduction:===== | ||
A Green self-revealing NCV of 10 CFR 50 Appendix B, Criterion V, Instructions, Procedures, and Drawings, was identified for the licensees failure to follow work management procedures. Specifically, the licensee failed to follow the conduct of maintenance procedure, MM-AA-100, Conduct of Maintenance, Revision 10, where maintenance personnel should use an assortment of techniques and tools to avoid errors during work execution. Attachment 6 step 1b outlines various human error prevention techniques that should have been used during the work execution including self checking and questioning attitude. | |||
=====Description:===== | =====Description:===== | ||
On December 10, 2014, the licensee was performing planned level transmitter calibrations for Level Channel I instrument loop (1-QS-L-100C) and Channel II instrument loop (1-QS-L-100D), for Unit 1 Refueling Water Storage Tank (RWST). The RWST is the suction source for all Emergency Core Cooling System pumps during the injection phase of a LOCA. There are three RWST level channels that feed the logic for auto-starting the Recirculation Spray (RS) system. The RS system is designed to lower containment pressure for a loss of coolant accident (LOCA) by spraying water from the sumps in containment back into the containment atmosphere. As an event progresses, the RWST level will decrease, and water collects in the containment sumps. | On December 10, 2014, the licensee was performing planned level transmitter calibrations for Level Channel I instrument loop (1-QS-L-100C) and Channel II instrument loop (1-QS-L-100D), for Unit 1 Refueling Water Storage Tank (RWST). | ||
The RWST is the suction source for all Emergency Core Cooling System pumps during the injection phase of a LOCA. There are three RWST level channels that feed the logic for auto-starting the Recirculation Spray (RS) system. The RS system is designed to lower containment pressure for a loss of coolant accident (LOCA) by spraying water from the sumps in containment back into the containment atmosphere. As an event progresses, the RWST level will decrease, and water collects in the containment sumps. | |||
The RS system is initiated with the receipt of Containment Pressure High-High signal coincident with RWST Level-Low. With Containment Pressure High-High, and two of the three RWST level channels indicate RWST level low, the actuation logic to auto-start the RS system is satisfied. | The RS system is initiated with the receipt of Containment Pressure High-High signal coincident with RWST Level-Low. With Containment Pressure High-High, and two of the three RWST level channels indicate RWST level low, the actuation logic to auto-start the RS system is satisfied. | ||
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TS 3.3.2, condition D, allows one RWST level channel to be inoperable at any time. | TS 3.3.2, condition D, allows one RWST level channel to be inoperable at any time. | ||
During maintenance or surveillance activities, to satisfy TS 3.3.2, condition D, only one level channel is placed in trip for calibration at a time. | During maintenance or surveillance activities, to satisfy TS 3.3.2, condition D, only one level channel is placed in trip for calibration at a time. However, on December 10, 2014, two required RWST level channels were inadvertently made inoperable due to concurrent channel level calibration work. The channel calibration work was briefed with emphasis to remove one level transmitter at a time; however there was no discussion about which channel calibration would be performed first: 1-QS-L-100C or 1-QS-L-100D. | ||
However, on December 10, 2014, two required RWST level channels were inadvertently made inoperable due to concurrent channel level calibration work. The channel calibration work was briefed with emphasis to remove one level transmitter at a time; however there was no discussion about which channel calibration would be performed first: 1-QS-L-100C or 1-QS-L-100D. | |||
Due to communication and coordination errors in the work control process, two work packages were worked simultaneously. The channel calibration work is conducted in two locations, the instrument rack and locally at the RWST. The technicians at the instrument rack proceeded to trip 1-QS-L-100D for calibration, per the TS3.3.2 condition D action. The technicians at the RWST proceeded to isolate and drain the second channel, 1-QS-L-100C, for calibration, resulting in a low level indication for another tripped channel. Because of the condition of two inoperable RWST level channels, the station no longer met the requirements of TS 3.3.2 and had to enter TS 3.0.3 because TS 3.3.2 does not contain an action for two inoperable RWST level channels. | Due to communication and coordination errors in the work control process, two work packages were worked simultaneously. The channel calibration work is conducted in two locations, the instrument rack and locally at the RWST. The technicians at the instrument rack proceeded to trip 1-QS-L-100D for calibration, per the TS3.3.2 condition D action. The technicians at the RWST proceeded to isolate and drain the second channel, 1-QS-L-100C, for calibration, resulting in a low level indication for another tripped channel. Because of the condition of two inoperable RWST level channels, the station no longer met the requirements of TS 3.3.2 and had to enter TS 3.0.3 because TS 3.3.2 does not contain an action for two inoperable RWST level channels. | ||
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Additionally, the station entered TS 3.6.7, condition F, for three or more RS subsystems inoperable. The required action for TS 3.6.7, condition F, is to enter LCO 3.0.3. The RS system is comprised of four subsystems, and the pump suction source is the sumps in containment. All four RS subsystems were inoperable because part of the actuation logic to auto-start the system was satisfied due to two tripped RWST level channels, meaning the RS system would actuate immediately on Containment Pressure High-High. In the condition described, the RWST level-low did not mean that the RWST water was in the sumps. The RS suction source was severely reduced. Therefore, if the RS system was actuated on a Containment Pressure High-High indication, the RS subsystem pumps would auto-start and there would not be sufficient water for pump suction. The RS pumps would operate with reduced suction source until manually turned off by the operators, and therefore, all four RS subsystems were inoperable. | Additionally, the station entered TS 3.6.7, condition F, for three or more RS subsystems inoperable. The required action for TS 3.6.7, condition F, is to enter LCO 3.0.3. The RS system is comprised of four subsystems, and the pump suction source is the sumps in containment. All four RS subsystems were inoperable because part of the actuation logic to auto-start the system was satisfied due to two tripped RWST level channels, meaning the RS system would actuate immediately on Containment Pressure High-High. In the condition described, the RWST level-low did not mean that the RWST water was in the sumps. The RS suction source was severely reduced. Therefore, if the RS system was actuated on a Containment Pressure High-High indication, the RS subsystem pumps would auto-start and there would not be sufficient water for pump suction. The RS pumps would operate with reduced suction source until manually turned off by the operators, and therefore, all four RS subsystems were inoperable. | ||
The inspectors reviewed Procedure MM-AA- | The inspectors reviewed Procedure MM-AA-100 Conduct of Maintenance, Revision 10, which provided the requirements for the conduct of maintenance process. Attachment 6 step 1b outlines various human error prevention techniques that should have been used during the work execution including self checking and questioning attitude. The inspectors concluded that the maintenance personnel did not use human error prevention tools when performing the maintenance. | ||
=====Analysis:===== | =====Analysis:===== | ||
The | The licensees failure to follow the conduct of maintenance procedure, MM-AA-100, Conduct of Maintenance, Revision 10, was a performance deficiency. | ||
dated June 19, 2012, and Appendix H | |||
Specifically, on December 10, 2014, maintenance personnel failed to effectively use human error prevention tools when performing the maintenance on the RWST level channels which resulted in a loss of the safety function of the RS system. The performance deficiency was more than minor because it was associated with the configuration control attribute of the Barrier Integrity cornerstone and adversely affected the cornerstone objective to ensure that the physical design barriers (fuel cladding, reactor coolant system, and containment) protect the public from radionuclide releases caused by accidents or events and is therefore a finding. Specifically, the RS system safety function was inadvertently rendered inoperable. The inspectors performed a Phase 1 analysis using the IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 3 Barrier Integrity Screening Questions, dated June 19, 2012, and Appendix H Containment Integrity Significance Determination Process, dated May 6, 2004, and determined the finding required a detailed risk evaluation because it involved the loss of safety function of the RS system. | |||
A detailed risk evaluation was performed in accordance with NRC Inspection Manual Chapter (IMC) 0609, Appendix A by a regional senior reactor analyst using the latest NRC North Anna SPAR model and Saphire risk program. The major analysis assumptions included: a thirty-two minute exposure interval, and a non-recoverable loss of both inside recirculation spray pumps and both outside recirculation pumps. The dominant risk sequence was a small break loss of coolant accident initiator, success of the reactor protection system, success of feedwater, success of high pressure injection, success of secondary side cooldown and failure of recirculation spray resulting in loss of core and containment heat removal capability. The risk was mitigated by the short exposure period. The risk evaluation result was an increase in core damage frequency of <1 E-6/year and an increase in large early release fraction of <1 E -7/year, a GREEN finding of very low safety significance. | A detailed risk evaluation was performed in accordance with NRC Inspection Manual Chapter (IMC) 0609, Appendix A by a regional senior reactor analyst using the latest NRC North Anna SPAR model and Saphire risk program. The major analysis assumptions included: a thirty-two minute exposure interval, and a non-recoverable loss of both inside recirculation spray pumps and both outside recirculation pumps. The dominant risk sequence was a small break loss of coolant accident initiator, success of the reactor protection system, success of feedwater, success of high pressure injection, success of secondary side cooldown and failure of recirculation spray resulting in loss of core and containment heat removal capability. The risk was mitigated by the short exposure period. The risk evaluation result was an increase in core damage frequency of <1 E-6/year and an increase in large early release fraction of <1 E -7/year, a GREEN finding of very low safety significance. | ||
The finding has a cross-cutting aspect in the area of human performance associated with the work management attribute because the organization failed to implement a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority. Furthermore, the licensee work process control includes the identification and management of risk commensurate to the work and the need for coordination with different groups or job activities. Specifically, due to poor communication and coordination between the Control Room and the technicians calibrating the RWST level channels, and amongst the team of technicians calibrating the RWST level transmitters, the RS system was inoperable [H.5]. | The finding has a cross-cutting aspect in the area of human performance associated with the work management attribute because the organization failed to implement a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority. Furthermore, the licensee work process control includes the identification and management of risk commensurate to the work and the need for coordination with different groups or job activities. Specifically, due to poor communication and coordination between the Control Room and the technicians calibrating the RWST level channels, and amongst the team of technicians calibrating the RWST level transmitters, the RS system was inoperable [H.5]. | ||
=====Enforcement:===== | =====Enforcement:===== | ||
Title 10 CFR Part 50, Appendix B, Criterion V, | Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, required, in part, that activities affecting quality be prescribed by documented instructions and procedures appropriate to the circumstances and shall be accomplished in accordance with these instructions and procedures. | ||
The | The licensees maintenance procedure, MM-AA-100, Conduct of Maintenance, Revision 10, requires maintenance personnel to use an assortment of techniques and tools to avoid errors during work execution. Attachment 6 step 1b outlines various human error prevention techniques that should have been used during the work execution including self checking and questioning attitude. | ||
Revision 10, requires maintenance personnel to use an assortment of techniques and | |||
Contrary to this requirement, the licensee failed to manage and accomplish activities affecting quality in accordance with documented procedures. Specifically, on December 10, 2014, maintenance personnel did not use human error prevention tools when performing the maintenance on the RWST level channels which resulted in the loss of the safety function of the RS system. Because it is of very low safety significance (Green), this violation is being treated as an NCV, consistent with Section 2.3.2.a of the NRC Enforcement Policy. The violation was entered into the licensees corrective action program as CR 567185. This non-cited violation is identified as NCV 05000338/2015001-01, Failure To Follow Procedure For RWST Instruments. | |||
Contrary to this requirement, the licensee failed to manage and accomplish activities affecting quality in accordance with documented procedures. Specifically, on December 10, 2014, maintenance personnel did not use human error prevention tools when performing the maintenance on the RWST level channels which resulted in the loss of the safety function of the RS system. Because it is of very low safety significance (Green), this violation is being treated as an NCV, consistent with Section 2.3.2.a of the NRC Enforcement Policy. The violation was | |||
{{a|1R13}} | {{a|1R13}} | ||
==1R13 Maintenance Risk Assessments and Emergent Work Control== | ==1R13 Maintenance Risk Assessments and Emergent Work Control== | ||
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: (2) management of risk; | : (2) management of risk; | ||
: (3) appropriate and necessary steps taken to plan and control the resulting emergent work activities upon identification of an unforeseen situation; and, | : (3) appropriate and necessary steps taken to plan and control the resulting emergent work activities upon identification of an unforeseen situation; and, | ||
: (4) adequate identification and resolution of maintenance risk assessments and emergent work problems. The inspectors verified that the licensee was in compliance with the requirements of 10 CFR 50.65 (a)(4) and the data output from the | : (4) adequate identification and resolution of maintenance risk assessments and emergent work problems. The inspectors verified that the licensee was in compliance with the requirements of 10 CFR 50.65 (a)(4) and the data output from the licensees safety monitor associated with the risk profile of Units 1 and 2. The inspectors reviewed the corrective action program to verify that deficiencies in risk assessments were being identified and properly resolved. | ||
* Emergent work for Unit 1 | * Emergent work for Unit 1 A Component Cooling Heat Exchange valve failure on January 11, 2015 | ||
* Outage safety review for Unit 1 forced outage on | * Outage safety review for Unit 1 forced outage on B main feed regulating valve operation on February 26, 2015 | ||
* Emergent work on Unit 2 | * Emergent work on Unit 2 C containment air recirculation fan | ||
* Maintenance activities during transition from Mode 4 to Mode 3 on March 25, 2015 | * Maintenance activities during transition from Mode 4 to Mode 3 on March 25, 2015 | ||
* Maintenance activities during transition from Mode 3 to Mode 2 on March 26, 2015 | * Maintenance activities during transition from Mode 3 to Mode 2 on March 26, 2015 | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R15}} | ||
{{a|1R15}} | |||
==1R15 Operability Determinations and Functionality Assessments== | ==1R15 Operability Determinations and Functionality Assessments== | ||
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====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed five operability determinations and functionality assessments, listed below, affecting risk-significant mitigating systems, to assess, as appropriate | The inspectors reviewed five operability determinations and functionality assessments, listed below, affecting risk-significant mitigating systems, to assess, as appropriate: (1)the technical adequacy of the evaluations; | ||
: (1) the technical adequacy of the evaluations; | |||
: (2) whether continued system operability was warranted; | : (2) whether continued system operability was warranted; | ||
: (3) whether other existing degraded conditions were considered as compensatory measures; | : (3) whether other existing degraded conditions were considered as compensatory measures; | ||
: (4) whether the compensatory measures, if involved, were in place, would work as intended, and were appropriately controlled; and, | : (4) whether the compensatory measures, if involved, were in place, would work as intended, and were appropriately controlled; and, | ||
: (5) where continued operability was considered unjustified, the impact on TS Limiting Conditions for Operation and the risk significance in accordance with the Significant Determination Process (SDP). The inspectors | : (5) where continued operability was considered unjustified, the impact on TS Limiting Conditions for Operation and the risk significance in accordance with the Significant Determination Process (SDP). The inspectors review included a verification that operability determinations (OD) were made as specified by procedure OP-AA-102, Operability Determination, Revision 12. Other documents reviewed are listed in the Attachment to this report. | ||
* Review of OD000604 Revision 2, Unit 2 Control Rod E-11 rod position indication signal stability | |||
Determination, | * Review of OD000605, OD to Evaluate N2 Leakage from 2-GN-TK-1B | ||
. Other documents reviewed are listed in the Attachment to this report. | * Review of OD000609, Need to Determine Operability of C RCS Loop with Flawed Elbow | ||
* Review of OD000604 Revision 2, | * Review of OD000611, Engineering to perform OD for U2 in light of Elbow Leakage in U1 RCS | ||
* Review of OD000605, | * Review of OD000612, AFW Check Valve Leakage (2-FW-70 & 2-FW-279) | ||
* Review of OD000609, | |||
* Review of OD000611, | |||
* Review of OD000612, | |||
====b. Findings==== | ====b. Findings==== | ||
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====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors performed a review regarding the | The inspectors performed a review regarding the licensees assessments and corrective actions for OWAs. The inspectors reviewed the cumulative effects of the licensees OWAs and procedure OP-AA-1700, Revision 6, Operations Aggregate Impact. The inspectors reviewed the data package associated with this procedure which included an evaluation of the cumulative effects of the OWAs on the operators ability to safely operate the plant and effectively respond to abnormal and emergency plant conditions. | ||
OP-AA-100, "Conduct of Operations," Revision 27. | The inspectors reviewed and monitored licensee planned and completed corrective actions to address underlying equipment issues causing the OWAs. The inspectors also evaluated OWAs against the requirements of the licensees corrective action program as specified in PI-AA-200, Corrective Action, Revision 23, 10 CFR 50, Appendix B, and OP-AA-100, "Conduct of Operations," Revision 27. | ||
====b. Findings and Observations==== | ====b. Findings and Observations==== | ||
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====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed the four completed permanent plant modification design change packages (DCP) listed below. The inspectors conducted a walkdown of the installation, discussed the desired improvement with system engineers, and reviewed the 10 CFR 50.59, Safety Review/Regulatory Screening, technical drawings, test plans and the modification package to assess the TS implications. Other documents reviewed are listed in the Attachment to this report. | The inspectors reviewed the four completed permanent plant modification design change packages (DCP) listed below. The inspectors conducted a walkdown of the installation, discussed the desired improvement with system engineers, and reviewed the 10 CFR 50.59, Safety Review/Regulatory Screening, technical drawings, test plans and the modification package to assess the TS implications. Other documents reviewed are listed in the Attachment to this report. | ||
* DC-NA-14-00004, | * DC-NA-14-00004, Install Tornado Missile Protection at U1/U2 AFW Pipe Tunnels. | ||
* DC-NA-14-00087, | * DC-NA-14-00087, BDB Aux Feedwater Pump House Flood Doors | ||
* DC-NA-14-00086, | * DC-NA-14-00086, BDB Aux Feedwater Pump House Flood Doors | ||
* DC-NA-13-00001, | * DC-NA-13-00001, Internals and Actuator Removal from SW screen wash AOV | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R19}} | ||
{{a|1R19}} | |||
==1R19 Post Maintenance Testing== | ==1R19 Post Maintenance Testing== | ||
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: (6) jumpers installed or leads lifted were properly controlled; | : (6) jumpers installed or leads lifted were properly controlled; | ||
: (7) test equipment was removed following testing; and, | : (7) test equipment was removed following testing; and, | ||
: (8) equipment was returned to the status required to perform in accordance with VPAP-2003, | : (8) equipment was returned to the status required to perform in accordance with VPAP-2003, Post Maintenance Testing Program, Revision 14. | ||
Revision 14. | * WO59102815326, Valve Gearbox Replacement for 1A Component Cooling HX Service Water (SW) Return No. 4 | ||
* WO59102815326, | * WO59102400280, Pump Repair for Hydro Test Pump 1-SI-P-2 | ||
* WO59102400280, | * WO59102813915, AMSAC Controller Module Replacement | ||
* WO59102813915, | * WO59102813478, 01-FW-FCV-1498 Repair Positioner | ||
* WO59102813478, | * 1-PT-83.12J, 1J Diesel Generator Test (Start by ESF Actuation) Followed by 24-Hour Run and Hot Restart Test | ||
* 1-PT-83.12J, | * WO59102832388/WO59102763186, 1-FW-P-2, Turbine Driven Auxiliary Feedwater Pump and Valve Test | ||
* WO59102832388/WO59102763186, | |||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R20}} | ||
{{a|1R20}} | |||
==1R20 Refueling and Other Outage Activities== | ==1R20 Refueling and Other Outage Activities== | ||
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====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed the Outage Safety Review (OSR) and contingency plans for the Unit 1 refueling outage, which began March 7, 2015, to confirm that the licensee had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing a plan that assured maintenance of defense-in-depth. The inspectors also confirmed that the licensee had mitigation/response strategies in place for any losses of key safety functions. Using NRC inspection procedure 71111.20, | The inspectors reviewed the Outage Safety Review (OSR) and contingency plans for the Unit 1 refueling outage, which began March 7, 2015, to confirm that the licensee had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing a plan that assured maintenance of defense-in-depth. The inspectors also confirmed that the licensee had mitigation/response strategies in place for any losses of key safety functions. Using NRC inspection procedure 71111.20, Refueling and Outage Activities, the inspectors observed portions of the refueling, and maintenance activities to verify that the licensee maintained defense-in-depth commensurate with the outage risk plan and applicable TS. The inspectors monitored licensee controls over the outage activities listed below. | ||
* Licensee configuration management, including daily outage reports, to evaluate maintenance of defense-in-depth commensurate with the OSR for key safety functions and compliance with the applicable TS when taking equipment out of service. | * Licensee configuration management, including daily outage reports, to evaluate maintenance of defense-in-depth commensurate with the OSR for key safety functions and compliance with the applicable TS when taking equipment out of service. | ||
* Implementation of clearance activities and confirmation that tags were properly hung and equipment appropriately configured to safely support the work or testing. | * Implementation of clearance activities and confirmation that tags were properly hung and equipment appropriately configured to safely support the work or testing. | ||
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====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
Unit 1 forced outage on December 22, 2014, due to a leak in an RCS drain pipe, which continued until January 1, 2015. During the forced outage period, the inspectors used NRC inspection procedure 71111.20, | Unit 1 forced outage on December 22, 2014, due to a leak in an RCS drain pipe, which continued until January 1, 2015. During the forced outage period, the inspectors used NRC inspection procedure 71111.20, Refueling and Outage Activities, to observe portions of the maintenance and startup activities to verify that the licensee maintained defense-in-depth commensurate with outage risk assessments and applicable TS. The inspectors reviewed licensee actions for the outage activities listed below. | ||
* Licensee configuration management, including daily outage reports, to evaluate defense-in-depth commensurate with the outage safety plan and compliance with the applicable TS when taking equipment out of service. | * Licensee configuration management, including daily outage reports, to evaluate defense-in-depth commensurate with the outage safety plan and compliance with the applicable TS when taking equipment out of service. | ||
* Controls over the status and configuration of electrical systems and switchyard to ensure that TS and outage safety plan requirements were met. | * Controls over the status and configuration of electrical systems and switchyard to ensure that TS and outage safety plan requirements were met. | ||
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====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
Unit 1 forced outage on February 26, 2015, due to failed circuit card for the | Unit 1 forced outage on February 26, 2015, due to failed circuit card for the B main feed regulator valve that went closed. During the forced outage period, the inspectors used NRC inspection procedure 71111.20, Refueling and Outage Activities, to observe portions of the maintenance and startup activities to verify that the licensee maintained defense-in-depth commensurate with outage risk assessments and applicable TS. The inspectors reviewed licensee actions for the outage activities listed below. | ||
* Licensee configuration management, including daily outage reports, to evaluate defense-in-depth commensurate with the outage safety plan and compliance with the applicable TS when taking equipment out of service. | * Licensee configuration management, including daily outage reports, to evaluate defense-in-depth commensurate with the outage safety plan and compliance with the applicable TS when taking equipment out of service. | ||
* Controls over the status and configuration of electrical systems and switchyard to ensure that TS and outage safety plan requirements were met. | * Controls over the status and configuration of electrical systems and switchyard to ensure that TS and outage safety plan requirements were met. | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R22}} | ||
{{a|1R22}} | |||
==1R22 Surveillance Testing== | ==1R22 Surveillance Testing== | ||
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For the seven surveillance tests listed below, the inspectors examined the test procedures, witnessed testing, or reviewed test records and data packages, to determine whether the scope of testing adequately demonstrated that the affected equipment was functional and operable, and that the surveillance requirements of TS were met. The inspectors also determined whether the testing effectively demonstrated that the systems or components were operationally ready and capable of performing their intended safety functions. | For the seven surveillance tests listed below, the inspectors examined the test procedures, witnessed testing, or reviewed test records and data packages, to determine whether the scope of testing adequately demonstrated that the affected equipment was functional and operable, and that the surveillance requirements of TS were met. The inspectors also determined whether the testing effectively demonstrated that the systems or components were operationally ready and capable of performing their intended safety functions. | ||
In-Service Test | In-Service Test: | ||
: | * 1-PT-75.2A, Service Water Pump (1-SW-P-1A) Quarterly Test, Revision 55 | ||
* 1-PT-75.2A, | * 2-PT-57.1B, Emergency Core Cooling Subsystem - Low Head Safety Injection Pump (2-SI-P-1B), Revision 60 RCS Leakage: | ||
* 2-PT-57.1B, | * 1-GOP-52.2A, Identifying Increased RCS Leakage, Revision 1 Containment Isolation Valve: | ||
: | * 1-PT-57.5A, Leakrate Test of 1-SI-P-1A and 1-SI-4, Revision 23 | ||
* 1-GOP-52.2A, | * 1-PT-57.5B, Leakrate Test of 1-SI-P-1B and 1-SI-21, Revision 25 Other Surveillance Tests: | ||
: | * 1-PT-14.1, Charging Pump 1-CH-P-1A, Revision 54 | ||
* 1-PT-57.5A, | * 2-PT-82J, 2J Emergency Diesel Generator Slow Start Test, Revision 57 | ||
* 1-PT-57.5B, | |||
: | |||
* 1-PT-14.1, | |||
* 2-PT-82J, | |||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. | ||
1EP6 Drill Evaluation | 1EP6 Drill Evaluation Emergency Preparedness (EP) Drill | ||
Emergency Preparedness (EP) Drill | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
On January 14, 2015, the inspectors reviewed and observed the performance of a drill that involved a Site Area Emergency where an automatic trip failed to shutdown the reactor and a faulted steam generator. The inspectors assessed emergency procedure usage, emergency plan classification, notifications, and the | On January 14, 2015, the inspectors reviewed and observed the performance of a drill that involved a Site Area Emergency where an automatic trip failed to shutdown the reactor and a faulted steam generator. The inspectors assessed emergency procedure usage, emergency plan classification, notifications, and the licensees identification and entrance of any problems into their corrective action program. This inspection evaluated the adequacy of the licensees conduct of the drill and performance critique. Exercise issues were captured by the licensee in their corrective action program as CRs. | ||
Requalification training deficiencies were captured within the operator training program. | Requalification training deficiencies were captured within the operator training program. | ||
Line 532: | Line 453: | ||
==RADIATION SAFETY== | ==RADIATION SAFETY== | ||
Cornerstones: | Cornerstones: Public Radiation Safety and Occupational Radiation Safety {{a|2RS1}} | ||
{{a|2RS1}} | |||
==2RS1 Radiological Hazard Assessment and Exposure Controls== | ==2RS1 Radiological Hazard Assessment and Exposure Controls== | ||
Line 540: | Line 459: | ||
Hazard Assessment and Instructions to Workers The inspectors discussed the possibility of changes to plant operations that could contribute to significant new radiological conditions since the last inspection with. The inspectors independently measured radiation dose rates or directly observed conduct of licensee radiation surveys for selected radiologically controlled areas (RCAs) during plant walkdowns. The inspectors reviewed survey records for several plant areas in the auxiliary building, rad waste processing and Independent Spent Fuel Storage Installation (ISFSI), including surveys for alpha emitters, airborne radioactivity, gamma surveys with a range of dose rate gradients, and pre-job and some post-job surveys for tasks. During facility tours, the inspectors directly observed labeling of radioactive material and postings for radiation areas, high radiation areas (HRAs) within the RCA of the auxiliary building and radioactive waste (radwaste) processing and storage locations. The inspectors reviewed radiation work permit (RWP) details to assess communication of radiological control requirements and current radiological conditions to workers for select jobs in HRAs. The inspector observed the oversight and coaching of workers in the containment exit undress area. | Hazard Assessment and Instructions to Workers The inspectors discussed the possibility of changes to plant operations that could contribute to significant new radiological conditions since the last inspection with. The inspectors independently measured radiation dose rates or directly observed conduct of licensee radiation surveys for selected radiologically controlled areas (RCAs) during plant walkdowns. The inspectors reviewed survey records for several plant areas in the auxiliary building, rad waste processing and Independent Spent Fuel Storage Installation (ISFSI), including surveys for alpha emitters, airborne radioactivity, gamma surveys with a range of dose rate gradients, and pre-job and some post-job surveys for tasks. During facility tours, the inspectors directly observed labeling of radioactive material and postings for radiation areas, high radiation areas (HRAs) within the RCA of the auxiliary building and radioactive waste (radwaste) processing and storage locations. The inspectors reviewed radiation work permit (RWP) details to assess communication of radiological control requirements and current radiological conditions to workers for select jobs in HRAs. The inspector observed the oversight and coaching of workers in the containment exit undress area. | ||
Control of Radioactive Material The inspectors observed surveys of material and personnel being released from the RCA using small article monitor, personnel contamination monitor, and portal monitor instruments, in accordance with procedures. Inspectors also observed instrument calibration stickers and observed and discussed setpoints for some instrumentation. The inspectors reviewed records of inventory selected sealed sources and discussed nationally tracked source transactions with licensee staff. | Control of Radioactive Material The inspectors observed surveys of material and personnel being released from the RCA using small article monitor, personnel contamination monitor, and portal monitor instruments, in accordance with procedures. | ||
Inspectors also observed instrument calibration stickers and observed and discussed setpoints for some instrumentation. The inspectors reviewed records of inventory selected sealed sources and discussed nationally tracked source transactions with licensee staff. | |||
Risk-Significant Radiation Areas, Hazard Control and Work Practices The inspectors evaluated access barrier effectiveness for selected Locked High Radiation Area (LHRA)locations and discussed procedural guidance and adherence for LHRA and Very High Radiation Area (VHRA) controls with health physics (HP) supervisors. The inspectors observed and evaluated controls for the storage of irradiated material within the spent fuel pool (SFP). Established radiological controls (including airborne controls) were evaluated for outage related work on Unit 1. In addition, the inspectors reviewed and discussed licensee controls for areas where dose rates could change significantly. | Risk-Significant Radiation Areas, Hazard Control and Work Practices The inspectors evaluated access barrier effectiveness for selected Locked High Radiation Area (LHRA)locations and discussed procedural guidance and adherence for LHRA and Very High Radiation Area (VHRA) controls with health physics (HP) supervisors. The inspectors observed and evaluated controls for the storage of irradiated material within the spent fuel pool (SFP). Established radiological controls (including airborne controls) were evaluated for outage related work on Unit 1. In addition, the inspectors reviewed and discussed licensee controls for areas where dose rates could change significantly. | ||
Through direct observations and interviews with licensee staff, the inspectors evaluated occupational workers | Through direct observations and interviews with licensee staff, the inspectors evaluated occupational workers adherence to selected RWPs and Health Physics Technicians (HPTs) proficiency in providing job coverage. Electronic dosimeter (ED) alarm set points and worker stay times were evaluated against area radiation survey results for selected entries into various high radiation areas and locked high radiation areas. The inspectors discussed the use of personnel dosimetry for multibadging work and areas with high dose gradients. The inspectors also evaluated worker response to dose and dose rate alarms during selected work activities. Inspectors reviewed RWPs for airborne radioactivity areas. | ||
Problem Identification and Resolution The inspectors reviewed and assessed Condition Reports (CRs) associated with radiological hazard assessment and control. The inspectors evaluated the licensees ability to identify and resolve the issues in accordance with licensee procedures. The inspectors also reviewed recent self-assessment results. | |||
report Attachment. | Radiation protection activities were evaluated against the requirements of Updated Final Safety Analysis Report (UFSAR) Section 12; Technical Specifications (TS) Sections 5.4 (Procedures) and 5.7 (High Radiation Areas); 10 CFR Parts 19 and 20; and approved licensee procedures. Licensee programs for monitoring materials and personnel released from the RCA were evaluated against 10 CFR Part 20 and IE Circular 81-07, Control of Radioactively Contaminated Material. Documents reviewed are listed in the report Attachment. | ||
====b. Findings==== | ====b. Findings==== | ||
Line 556: | Line 475: | ||
==OTHER ACTIVITIES== | ==OTHER ACTIVITIES== | ||
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity | Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity {{a|4OA1}} | ||
{{a|4OA1}} | |||
==4OA1 Performance Indicator (PI) Verification== | ==4OA1 Performance Indicator (PI) Verification== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors performed a periodic review of the three Unit 1 and 2 PIs listed below to assess the accuracy and completeness of the submitted data and whether the performance indicators were calculated in accordance with the guidance contained in Nuclear Energy Institute (NEI) 99-02, | The inspectors performed a periodic review of the three Unit 1 and 2 PIs listed below to assess the accuracy and completeness of the submitted data and whether the performance indicators were calculated in accordance with the guidance contained in Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7. The inspection was conducted in accordance with NRC inspection procedure 71151, Performance Indicator Verification. Specifically, the inspectors reviewed the Unit 1 and Unit 2 data reported to the NRC for the period January 1, 2014 through December 31, 2014. Documents reviewed included applicable NRC inspection reports, licensee event reports, operator logs, station performance indicators, and related CRs. | ||
* Unplanned Scrams per 7000 Critical Hours (IE01) | * Unplanned Scrams per 7000 Critical Hours (IE01) | ||
* Unplanned Transients per 7000 Critical Hours(IE03) | * Unplanned Transients per 7000 Critical Hours(IE03) | ||
Line 569: | Line 486: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. | ||
{{a|4OA2}} | |||
{{a|4OA2}} | |||
==4OA2 Problem Identification and Resolution== | ==4OA2 Problem Identification and Resolution== | ||
===.1 Review of Items Entered into the Corrective Action Program=== | ===.1 Review of Items Entered into the Corrective Action Program=== | ||
As required by NRC inspection procedure 71152, | As required by NRC inspection procedure 71152, Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensees CAP. This review was accomplished by reviewing daily CR report summaries and periodically attending daily CR Review Team meetings. | ||
===.2 Annual Sample: | ===.2 Annual Sample: Review of CR568624, The normal level controller for Unit 2 1A=== | ||
Review of CR568624, | |||
feedwater heater has failed | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors performed a review regarding the | The inspectors performed a review regarding the licensees assessments and corrective actions for CR568624, The normal level controller for Unit 2 1A feedwater heater has failed, to ensure that the full extent of the issue was identified, an appropriate evaluation was performed, and appropriate corrective actions were specified and prioritized. The inspectors also evaluated the CR against the requirements of the licensees CAP as specified in licensee procedure, PI-AA-200, Corrective Action Program, Revision 23 and 10 CFR 50, Appendix B. | ||
was performed, and appropriate corrective actions were specified and prioritized. The inspectors also evaluated the CR against the requirements of the | |||
====b. Findings and Observations==== | ====b. Findings and Observations==== | ||
No findings were identified. In general, the inspectors verified that the licensee had identified problems at an appropriate threshold and entered them into the CAP database, and had proposed or implemented appropriate corrective actions. | No findings were identified. In general, the inspectors verified that the licensee had identified problems at an appropriate threshold and entered them into the CAP database, and had proposed or implemented appropriate corrective actions. | ||
===.3 Annual Sample: | ===.3 Annual Sample: Review of CR567185, Two channels of U1 RWST level removed from=== | ||
Review of CR567185, | |||
service during calibrations, and CR567188, North Anna Unit 1 Entered TS 3.0.3 due to 2 inoperable RWST Level Transmitters | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors performed a review regarding the | The inspectors performed a review regarding the licensees assessments and corrective actions for CR567185, Two channels of U1 RWST level removed from service during calibrations, and CR567188, North Anna Unit 1 Entered TS 3.0.3 due to 2 inoperable RWST Level Transmitters, to ensure that the full extent of the issue was identified, an appropriate evaluation was performed, and appropriate corrective actions were specified and prioritized. The inspectors also evaluated the CR against the requirements of the licensees CAP as specified in licensee procedure, PI-AA-200, Corrective Action Program, Revision 23, and 10 CFR 50, Appendix B. | ||
Program, | |||
====b. Findings and Observations==== | ====b. Findings and Observations==== | ||
In general, the inspectors verified that the licensee had identified problems at an appropriate threshold and entered them into the CAP database, and had proposed or implemented appropriate corrective actions. See Section 1R12 for details of finding. | In general, the inspectors verified that the licensee had identified problems at an appropriate threshold and entered them into the CAP database, and had proposed or implemented appropriate corrective actions. See Section 1R12 for details of finding. | ||
===.4 Annual Sample: | ===.4 Annual Sample: Review of CR568497, 3CND-P3 Oil bubbler low at 1/16th full=== | ||
Review of CR568497, | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors performed a review regarding the | The inspectors performed a review regarding the licensees assessments and corrective actions for CR568497, 3CND-P3 Oil bubbler low at 1/16th full, to ensure that the full extent of the issue was identified, an appropriate evaluation was performed, and appropriate corrective actions were specified and prioritized. The inspectors also evaluated the CR against the requirements of the licensees CAP as specified in licensee procedure, PI-AA-200, Corrective Action Program, Revision 23, and 10 CFR 50, Appendix B. | ||
====b. Findings and Observations==== | ====b. Findings and Observations==== | ||
Line 617: | Line 530: | ||
The 1A FW Heater Normal Level Controller failed and the normal level control/cascade valve for Unit 2 1A FW Heater failed closed and was unable to be adjusted. The licensee commenced ramp down for the unit to maintain reactor power. The inspectors reviewed the problem resolution documents and the licensee actions taken to ensure appropriate corrective actions were specified and prioritized. Documents reviewed are listed in the Attachment to this report. | The 1A FW Heater Normal Level Controller failed and the normal level control/cascade valve for Unit 2 1A FW Heater failed closed and was unable to be adjusted. The licensee commenced ramp down for the unit to maintain reactor power. The inspectors reviewed the problem resolution documents and the licensee actions taken to ensure appropriate corrective actions were specified and prioritized. Documents reviewed are listed in the Attachment to this report. | ||
===.2 (Closed) LER 05000338/2014-002-00: | ===.2 (Closed) LER 05000338/2014-002-00: Inadvertent Loss of Vital Instrumentation During=== | ||
Inadvertent Loss of Vital Instrumentation During | |||
On December 10, 2014, with Unit 1 in Mode 1 at 100 percent power, Station technicians commenced scheduled periodic channel calibrations of level transmitters for the Unit 1 Refueling Water Storage Tank Level Channel I instrument loop and Channel II instrument loop. At 1344 hours, two channels of the Unit 1 Refueling Water Storage Tank (RWST) level instrumentation were inadvertently removed from service at the same time during maintenance. Operations personnel responded by entering abnormal procedure 1-AP-3, | Maintenance Due to Personnel Error On December 10, 2014, with Unit 1 in Mode 1 at 100 percent power, Station technicians commenced scheduled periodic channel calibrations of level transmitters for the Unit 1 Refueling Water Storage Tank Level Channel I instrument loop and Channel II instrument loop. At 1344 hours, two channels of the Unit 1 Refueling Water Storage Tank (RWST) level instrumentation were inadvertently removed from service at the same time during maintenance. Operations personnel responded by entering abnormal procedure 1-AP-3, Loss of Vital Instrumentation. The licensee also entered TS 3.0.3 due to two channels being inoperable that affect Recirculation Spray (RS) pump auto-start logic. At 1356 hours, both level indications returned to normal. At 1417 hours, Channel II was declared operable and TS 3.0.3 was cleared. At 1439, Channel I was declared operable and TS actions were cleared. | ||
Had a containment depressurization actuation (CDA) occurred during this time, accident mitigation may have been impacted. The RS pumps would have started without sufficient suction water, however the control room could promptly reset the CDA signal | Had a containment depressurization actuation (CDA) occurred during this time, accident mitigation may have been impacted. The RS pumps would have started without sufficient suction water, however the control room could promptly reset the CDA signal and manually shutdown the RS pumps to prevent damage. The event posed no significant safety implications and the health and safety of the public were not affected by this event. | ||
and manually shutdown the RS pumps to prevent damage. The event posed no significant safety implications and the health and safety of the public were not affected | |||
by this event. | |||
The cause of the event was personnel error. Station technicians failed to assess risk associated with the RWST level calibration tasks. Inattention as a result of repetition and/or becoming complacent and overconfident with the job task caused the team not to use human performance tools to mitigate the errors. Completed interim actions included removing the qualifications of the individuals involved until remediation was conducted; performing a stand down to ensure lessons learned are integrated into the daily work activities and department standards and expectations were reinforced; and supervisors have increased oversight for pre-job briefs and are maintaining field presence to ensure high rick error likely tasks are briefed adequately, barriers and defenses used and standards and expectations reinforced. | The cause of the event was personnel error. Station technicians failed to assess risk associated with the RWST level calibration tasks. Inattention as a result of repetition and/or becoming complacent and overconfident with the job task caused the team not to use human performance tools to mitigate the errors. Completed interim actions included removing the qualifications of the individuals involved until remediation was conducted; performing a stand down to ensure lessons learned are integrated into the daily work activities and department standards and expectations were reinforced; and supervisors have increased oversight for pre-job briefs and are maintaining field presence to ensure high rick error likely tasks are briefed adequately, barriers and defenses used and standards and expectations reinforced. | ||
This issue is in the | This issue is in the licensees CAP as CR567185, Two channels of U1 RWST level removed from service during maintenance. See Section 1R12 for details of finding. | ||
{{a|4OA6}} | {{a|4OA6}} | ||
Line 637: | Line 545: | ||
===Exit Meeting Summary=== | ===Exit Meeting Summary=== | ||
On April 22, 2015 , the resident inspectors presented the inspection results to Mr. G. | On April 22, 2015, the resident inspectors presented the inspection results to Mr. G. | ||
report. | Bischof and other members of the staff, who acknowledged the findings. The inspectors verified no proprietary information was retained by the inspectors or documented in this report. | ||
ATTACHMENT: | ATTACHMENT: SUPPPLEMENTARY INFORMATION | ||
=SUPPLEMENTARY INFORMATION= | =SUPPLEMENTARY INFORMATION= | ||
Line 649: | Line 557: | ||
===Licensee personnel=== | ===Licensee personnel=== | ||
: | : | ||
: [[contact::M. Becker]], Manager, Nuclear Outage and Planning | : [[contact::M. Becker]], Manager, Nuclear Outage and Planning | ||
: [[contact::R. Britt]], BACCP Lead | : [[contact::R. Britt]], BACCP Lead | ||
: [[contact::G. Bischof]], Site Vice President | : [[contact::G. Bischof]], Site Vice President | ||
: [[contact::C. Cherry]], ISI Program Manager | : [[contact::C. Cherry]], ISI Program Manager | ||
: [[contact::B. Derreberry]], ISI/NDE Supervisor | : [[contact::B. Derreberry]], ISI/NDE Supervisor | ||
: [[contact::B. Evans]], Manager Radiation Protection | : [[contact::B. Evans]], Manager Radiation Protection | ||
: [[contact::B. Gaspar]], Manager, Nuclear Site Services | : [[contact::B. Gaspar]], Manager, Nuclear Site Services | ||
: [[contact::R. Hanson]], Manager, Nuclear Protection Services | : [[contact::R. Hanson]], Manager, Nuclear Protection Services | ||
: [[contact::E. Hendrixson]], Director, Nuclear Site Engineering | : [[contact::E. Hendrixson]], Director, Nuclear Site Engineering | ||
: [[contact::L. Hilbert]], Director, Nuclear Station Safety & Licensing | : [[contact::L. Hilbert]], Director, Nuclear Station Safety & Licensing | ||
: [[contact::J. Jenkins]], Manager, Nuclear Maintenance | : [[contact::J. Jenkins]], Manager, Nuclear Maintenance | ||
: [[contact::P. Kemp]], Supervisor, Station Licensing | : [[contact::P. Kemp]], Supervisor, Station Licensing | ||
: [[contact::H. Le]], Engineering Programs Manager, | : [[contact::H. Le]], Engineering Programs Manager, | ||
: [[contact::J. Leberstien]], Technical Advisor, Licensing | : [[contact::J. Leberstien]], Technical Advisor, Licensing | ||
: [[contact::A. Maly]], Supervisor Technical Services | : [[contact::A. Maly]], Supervisor Technical Services | ||
: [[contact::F. Mladen]], Plant Manager | : [[contact::F. Mladen]], Plant Manager | ||
: [[contact::N. Nicholson]], Health Physicist III | : [[contact::N. Nicholson]], Health Physicist III | ||
: [[contact::T. Pastor]], Supervisor Radiation Protection Technical Services | : [[contact::T. Pastor]], Supervisor Radiation Protection Technical Services | ||
: [[contact::J. Plossl]], Supervisor, Nuclear Station Procedures | : [[contact::J. Plossl]], Supervisor, Nuclear Station Procedures | ||
: [[contact::M. Sartain]], Nuclear Engineering Vice President | : [[contact::M. Sartain]], Nuclear Engineering Vice President | ||
: [[contact::J. Schleser]], Manager, Nuclear Organizational Effectiveness | : [[contact::J. Schleser]], Manager, Nuclear Organizational Effectiveness | ||
: [[contact::R. Simmons]], Supervisor Radiation Protection Operations | : [[contact::R. Simmons]], Supervisor Radiation Protection Operations | ||
: [[contact::J. Slattery]], Manager, Nuclear Operations | : [[contact::J. Slattery]], Manager, Nuclear Operations | ||
: [[contact::R. Stack]], NDE Lead | : [[contact::R. Stack]], NDE Lead | ||
: [[contact::W. Standley]], Manager, Nuclear Training | : [[contact::W. Standley]], Manager, Nuclear Training | ||
: [[contact::J. Swenson]], Site Welding Engineer | : [[contact::J. Swenson]], Site Welding Engineer | ||
: [[contact::M. Whalen]], Technical Advisor, Licensing | : [[contact::M. Whalen]], Technical Advisor, Licensing | ||
==LIST OF ITEMS== | ==LIST OF ITEMS== | ||
Line 682: | Line 590: | ||
===Opened and Closed=== | ===Opened and Closed=== | ||
: 05000338/2015001-01 NCV Failure To Follow Procedure For RWST | : 05000338/2015001-01 NCV Failure To Follow Procedure For RWST Instruments (Section 1R12) | ||
Instruments (Section 1R12) | |||
===Closed=== | ===Closed=== | ||
: 05000338/2014-002-00 LER Inadvertent Loss of Vital Instrumentation During Maintenance Due to Personnel Error (Section 4OA3.2) | |||
===Discussed=== | ===Discussed=== | ||
None | None | ||
==LIST OF DOCUMENTS REVIEWED== | ==LIST OF DOCUMENTS REVIEWED== | ||
}} | }} |
Latest revision as of 04:16, 20 December 2019
ML15128A363 | |
Person / Time | |
---|---|
Site: | North Anna |
Issue date: | 05/08/2015 |
From: | Steven Rose NRC/RGN-II/DRP/RPB5 |
To: | Heacock D Virginia Electric & Power Co (VEPCO) |
References | |
IR 2015001 | |
Download: ML15128A363 (39) | |
Text
UNITED STATES May 8, 2015
SUBJECT:
NORTH ANNA POWER STATION - NRC INTEGRATED INSPECTION REPORT 05000338/2015001 and 05000339/2015001
Dear Mr. Heacock:
On March 31, 2015, the U. S. Nuclear Regulatory Commission (NRC) completed an inspection at your North Anna Power Station, Units 1 and 2. On April 22, 2015, the NRC inspectors discussed the results of this inspection with Mr. G. Bischof and other members of your staff.
Inspectors documented the results of this inspection in the enclosed inspection report.
Nuclear Regulatory Commission inspectors documented one self-revealing finding of very low safety significance (Green) in this report which was determined to involve a violation of NRC requirements. The NRC is treating this finding as a non-cited violation (NCV) consistent with Section 2.3.2 of the NRC Enforcement Policy.
If you wish to contest this NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN:
Document Control Desk, Washington, DC 20555-001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the North Anna Power Station.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the North Anna Power Station. In accordance with Title 10 Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding, of the NRC's "Agency Rules of Practice and Procedure," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS) component of NRC's Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Steven D. Rose, Chief Reactor Projects Branch 5 Division of Reactor Projects Docket Nos.: 05000338, 05000339 License Nos.: NPF-4, NPF-7
Enclosure:
IR 05000338/2015001 and 05000339/2015001 w/ Attachment: Supplementary Information
REGION II==
Docket Nos: 50-338, 50-339 License Nos: NPF-4, NPF-7 Report No: 05000338/2015001 and 05000339/2015001 Licensee: Virginia Electric and Power Company (VEPCO)
Facility: North Anna Power Station, Units 1 & 2 Location: Mineral, Virginia 23117 Dates: January 1, 2015 through March 31, 2015 Inspectors: G.Kolcum, Senior Resident Inspector G. Skaggs Ryan, Resident Inspector R. Carrion, Senior Reactor Engineer, Section 1R08 R. Hamilton, Senior Health Physicist, Section 2RS1 Approved by: Steven D. Rose, Chief Reactor Projects Branch 5 Division of Reactor Projects Enclosure
SUMMARY
IR 05000338/2015-001, 05000339/2015-001; 01/01/2015 - 03/31/2015; North Anna Power
Station, Units 1 and 2. Maintenance Effectiveness.
The report covered a three-month period of inspection by resident inspectors and senior operations engineers from the region. One self-revealing finding was identified and was determined to be a non-cited violation (NCV). The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,
Significance Determination Process (SDP). The cross-cutting aspect was determined using IMC 0310, Components Within the Cross Cutting Areas. All violations of NRC requirements are dispositioned in accordance with the NRCs Enforcement Policy, dated February 5, 2015.
The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 5, dated February 2014.
Cornerstone: Barrier Integrity
- Green.
A self-revealing NCV of 10 CFR 50 Appendix B, Criterion V, Instructions,
Procedures, and Drawings, was identified for the licensees failure to follow work management procedures. Specifically, the licensee failed to follow the conduct of maintenance procedure, MM-AA-100, Conduct of Maintenance, Revision 10, where maintenance personnel should use an assortment of techniques and tools to avoid errors during work execution. Attachment 6 step 1b outlines various human error prevention techniques that should have been used during the work execution including self checking and questioning attitude. This issue was entered this into the licensees corrective action program as CR 567185.
The licensees failure to follow the conduct of maintenance procedure, MM-AA-100,
Conduct of Maintenance, Revision 10, was a performance deficiency. Specifically, on December 10, 2014, maintenance personnel failed to effectively use human error prevention tools when performing the maintenance on the Refueling Water Storage Tank (RWST) level channels which resulted in a loss of the safety function of the Recirculation Spray (RS)system. The performance deficiency was more than minor because it was associated with the configuration control attribute of the Barrier Integrity cornerstone and adversely affected the cornerstone objective to ensure that the physical design barriers (fuel cladding, reactor coolant system, and containment) protect the public from radionuclide releases caused by accidents or events and is therefore a finding. Specifically, the RS system safety function was inadvertently rendered inoperable. The inspectors performed a Phase 1 analysis using the IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 3 Barrier Integrity Screening Questions, dated June 19, 2012 and Appendix H, Containment Integrity Significance Determination Process, dated May 6, 2004, and determined the finding required a detailed risk evaluation because it involved the loss of safety function of the RS system.
A detailed risk evaluation was performed in accordance with NRC Inspection Manual Chapter (IMC) 0609, Appendix A by a regional senior reactor analyst using the latest NRC North Anna SPAR model and Saphire risk program. The major analysis assumptions included: a thirty-two minute exposure interval, and a non-recoverable loss of both inside recirculation spray pumps and both outside recirculation pumps. The dominant risk sequence was a small break loss of coolant accident initiator, success of the reactor protection system, success of feedwater, success of high pressure injection, success of secondary side cooldown and failure of recirculation spray resulting in loss of core and containment heat removal capability. The risk was mitigated by the short exposure period.
The risk evaluation result was an increase in core damage frequency of <1 E-6/year and an increase in large early release fraction of <1 E -7/year, a GREEN finding of very low safety significance.
The finding has a cross-cutting aspect in the area of human performance associated with the work management attribute because the organization failed to implement a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority. Furthermore, the licensee work process control includes the identification and management of risk commensurate to the work and the need for coordination with different groups or job activities. Specifically, due to poor communication and coordination between the Control Room and the technicians calibrating the RWST level channels, and amongst the team of technicians calibrating the RWST level transmitters, the RS system was inoperable [H.5] (1R12).
REPORT DETAILS
Summary of Plant Status
Unit 1 entered a forced outage due to a leak in a Reactor Coolant System (RCS) drain pipe on December 22, 2014. Unit 1 began the period at full Rated Thermal Power (RTP) and operated at full power until the Unit experienced an automatic trip on February 26, 2015, due to a circuit card failure on B main feed regulating valve for B steam generator level control. Unit 1 restarted on February 28, 2015, and returned to ninety percent power on March 2, 2015. Unit 1 went off line on March 7, 2015, for the planned spring refueling outage. Unit 1 started up on March 28 and returned online March 29, 2015, and returned to full RTP on March 30, 2015.
Unit 2 began the period at full RTP and operated at full power for the entire report period.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection
.1 External Flooding
a. Inspection Scope
The inspectors assessed the external flood vulnerability of the North Anna for the fuel transfer pump building. The inspectors verified the condition of the emergency flood protection dike between the service water pond, and the plant and related drainage ditches and culverts, in addition to the west side flood protection dike. The inspectors also reviewed applicable station procedures and design documents to assess proper surveillance and maintenance for external flood protection features.
b. Findings
No findings were identified.
.2 Seasonal Susceptibilities
a. Inspection Scope
The inspectors reviewed the licensees adverse weather preparations for cold weather operations specified in 0-GOP-4, Cold Weather Operations, Revision 56, 0-GOP-4.2, Extreme Cold Weather Operations, Revision 36, and 0-GOP-4.2A, Extreme Cold Weather Daily Checks, Revision 8, as well as the licensees corrective action data base for cold weather related issues. The inspectors walked down the risk-significant areas listed below on two occasions to verify compliance with procedural requirements and to verify that the specified actions provided the necessary protection for the applicable structures, systems, or components (SSCs). The inspectors reviewed the licensees corrective action program (CAP) database to verify that weather related problems due to temperature were being identified at the appropriate level, entered into the CAP, and appropriately resolved.
- Unit 1 and 2 Emergency Diesel Generator Rooms and Station Blackout (SBO) Diesel on January 7, 2015 with weather in the teens
- Unit 1 and 1 Emergency Diesel Generator room and the SBO Emergency Diesel Generator on February 15, 2015 with temperatures below 15 degrees Fahrenheit
b. Findings
No findings were identified.
.3 Impending Adverse Weather Conditions
a. Inspection Scope
The inspectors performed a site specific weather related inspection due to anticipated adverse weather conditions. On February 2, 2015, the inspectors reviewed the licensee response to high wind warnings of 25 to 35 miles an hour with gusts up to 40 miles an hour for the area. Specifically, the inspectors reviewed licensee adverse weather response procedures, including 0-AP-41, Severe Weather Conditions, Revision 61, and site preparations including work activities that could impact the overall maintenance risk assessments.
b. Findings
No findings were identified.
1R04 Equipment Alignment
Partial Walkdowns
a. Inspection Scope
The inspectors conducted seven equipment alignment partial walkdowns, listed below, to evaluate the operability of selected redundant trains or backup systems with the other train or system inoperable or out of service. The inspectors reviewed the functional systems descriptions, Updated Final Safety Analysis Report (UFSAR), system operating procedures, and Technical Specifications (TS) to determine correct system lineups for the current plant conditions. The inspectors performed walkdowns of the systems to verify the operability of a redundant or backup system/train or a remaining operable system/train with a high risk significance for the current plant configuration (considering out-of-service, inoperable, or degraded condition); or a risk-significant system/train that was recently realigned following an extended system outage, maintenance, modification, or testing; or a risk-significant single-train system. The inspector conducted the reviews to ensure that critical components were properly aligned, and to identify any discrepancies which could affect operability of the redundant train or backup system.
- Unit 1 Auxiliary Feedwater (AFW) Terry Turbine during startup preparations after refueling
- Unit 1 Motor-Driven AFW trains A and B during startup preparations after refueling
- 1H and 1J Emergency Diesel Generators (EDGs) during startup preparations after refueling
- Unit 1 component cooling heat exchangers after maintenance on A component cooling heat exchanger
- 1H EDG fuel oil transfer system
- Unit 1 charging pumps during maintenance on B charging pump
- Unit 2 B low head safety injection pump
b. Findings
No findings were identified
.2 Complete Walkdown
a. Inspection Scope
The inspectors performed a detailed walkdown and inspection of the Unit 1 AFW system to assess proper alignment and to identify discrepancies that could impact its availability and functional capacity. The inspectors assessed the physical condition and position of each recirculation spray and casing cooling valve, whether manual, power operated or automatic, to ensure correct positioning of the valves. The inspection also included a review of the alignment and the condition of support systems including fire protection, room ventilation, and emergency lighting. Equipment deficiency tags were reviewed and the condition of the system was discussed with the engineering personnel.
b. Findings
No findings were identified.
1R05 Fire Protection
.1 Quarterly Fire Protection Walkdowns
a. Inspection Scope
The inspectors conducted focused tours of the five areas listed below that are important to reactor safety to verify the licensees implementation of fire protection requirements as described in fleet procedures CM-AA-FPA-100, Fire Protection/Appendix R (Fire Safe Shutdown) Program, Revision 10, CM-AA-FPA-101, Control of Combustible and Flammable Materials, Revision 6, and CM-AA-FPA-102, Fire Protection and Fire Safe Shutdown Review and Preparation Process and Design Change Process, Revision 5.
The inspectors evaluated, as appropriate, conditions related to:
- (1) licensee control of transient combustibles and ignition sources;
- (2) the material condition, operational status, and operational lineup of fire protection systems, equipment, and features; and,
- (3) the fire barriers used to prevent fire damage or fire propagation. Other documents reviewed are listed in the Attachment to this report.
- Main Control Room
- Unit 1 Emergency Switchgear Room
- Emergency Diesel Generators 1H and 2H
- Emergency Diesel Generators 1J and 2J
- Battery Rooms
b. Findings
No findings were identified.
1R06 Flood Protection Measures
a. Inspection Scope
The inspectors assessed the internal flooding vulnerability of the two flood areas listed below with respect to adjacent safety-related areas to verify that the flood protection barriers and equipment were being maintained consistent with the UFSAR. The licensees corrective action documents were reviewed to verify that corrective actions with respect to flood-related items identified in condition reports were adequately addressed. The inspectors conducted a field survey of the selected areas to evaluate the adequacy of flood barriers, and floor drains to protect the equipment, as well as their overall material condition.
- Unit 1 AFW Pump House
- Fuel Oil Pump House
b. Findings
No findings were identified.
1R07 Heat Sink Performance
System Heat Exchangers
a. Inspection Scope
The inspectors selected the risk significant Unit 1 B Charging Pump Lube Oil Heat Exchangers (HXs) for the 1B Gear Box Lube Oil Cooler and reviewed inspection records, test results, maintenance work orders, and other documentation to ensure that deficiencies which could mask or degrade performance were identified and corrected.
The test procedures and records were also reviewed to verify that they were consistent with Generic Letter 89-13 licensee commitments, and Electric Power Research Institute (EPRI) Heat Exchanger Performance Monitoring Guidelines. In addition, the inspectors reviewed inspection documentation of the related service water piping to assess general material condition and to identify any degraded conditions. Documents reviewed included Virginia Power Administrative Procedure (VPAP) -0811, Service Water Inspection and Maintenance Program, Revision 6, and licensee procedure ER-AA-HTX-1003, Heat Exchanger Monitoring and Assessment, Revision 6.
b. Findings
No findings were identified.
1R08 Inservice Inspection Activities
a. Inspection Scope
Non-Destructive Examination Activities and Welding Activities From March 19 - 23, 2015, the inspectors conducted an onsite review of the implementation of the licensees inservice inspection (ISI) program for monitoring degradation of the reactor coolant system boundary, risk-significant piping and component boundaries, and containment boundaries in Unit 1.
The inspectors either directly observed or reviewed the following non-destructive examinations (NDEs) mandated by the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (Code of Record: 2004 Edition with 2006 Addenda) to evaluate compliance with the ASME Code,Section XI and Section V requirements, and if any indications or defects were detected, to evaluate if they were dispositioned in accordance with the ASME Code or an NRC-approved alternative requirement. (Note: The Code of Record for IWE and IWL is the 2001 Edition with 2003 Addenda.) The inspectors also reviewed the qualifications of the NDE technicians performing the examinations, to determine whether they were current and in compliance with the ASME Code requirements.
- Ultrasonic Testing (UT), Weld 11715-WMKS-0102C/16-WFPD-22/18A, Elbow to Nozzle Weld, Class 2 (observed)
- Magnetic Particle Testing (MT), Weld 11715-WMKS-RC-E2/1-RC-E-2/8, Pressurizer Integral Attachment (reviewed)
- Visual Testing (VT)-15-024, Restraint 11715-WMKS-0103AT/2-CH-96/R24 (reviewed)
- VT-15-032, Restraint 11715-WMKS-01031B/32-SHP-1/R44 (reviewed)
- Phased array UT, Weld 11715-WMKS-RC-E-1A.2/29-RC-1/N-SE29IN, A SG Hot Leg WOR (Weld Overlay Repair) (reviewed)
The inspectors reviewed the following welding activities to evaluate compliance with procedures, and the ASME Code Section XI and Section IX requirements. Specifically, the inspectors reviewed the associated work orders, repair and replacement plans, weld data sheets, welding procedures, procedure qualification records, welder performance qualification records, and NDE reports.
- Replacement of 3" Velan Check Valve, Class 1 (reviewed)
- Canopy Seal Weld Repair, 1-RC-64, Class 1 (reviewed)
- Valve Replacement of 1-CH-302, 4B Seal Water Injection Filter Inlet Isolation Valve (reviewed)
- Permanent Shielding for Charging Letdown Piping (reviewed)
- Replacement of 2 Elbow on C Loop Drain Line. (reviewed)
During non-destructive surface and volumetric examinations performed since the previous refueling outage, the licensee did not identify any relevant indications that were analytically evaluated and accepted for continued service; therefore, no NRC review was completed for this inspection procedure attribute.
Pressurized Water Reactor Vessel Upper Head Penetration Inspection Activities The inspectors verified that for the Unit 1 vessel head, a bare metal visual (BMV)examination and a volumetric examination were not required during this outage, in accordance with the requirements of ASME Code Case N-729-1 and 10 CFR 50.55a(g)(6)(ii)(D). The inspectors also reviewed the licensees Alloy 600 Management Plan, to verify the implemented strategy provides reasonable assurance that plant safety will be maintained.
The licensee did not identify any relevant indications that were accepted for continued service during the previous BMV exams. Additionally, the licensee did not perform any welding repairs to the vessel head penetrations since the beginning of the last Unit 1 refueling outage; therefore, no NRC review was completed for these inspection procedure attributes.
Boric Acid Corrosion Control Inspection Activities The inspectors reviewed the licensees boric acid corrosion control program (BACCP)activities to ensure implementation with commitments made in response to NRC Generic Letter 88-05, Boric Acid Corrosion of Carbon Steel Reactor Pressure Boundary Components in PWR Plants, and applicable industry guidance documents. Specifically, the inspectors performed an onsite record review of procedures, and the results of the licensees containment walkdown inspections performed during the current spring refueling outage. The inspectors also interviewed the BACCP owner, conducted an independent walkdown of containment to evaluate compliance with licensees BACCP requirements, and verified that degraded or non-conforming conditions, such as boric acid leaks, were properly identified and corrected in accordance with the licensees BACCP, and corrective action program (CAP). The inspectors also reviewed the BACCP health reports since the last Unit 1 outage to evaluate program trends.
The inspectors reviewed the following engineering evaluations completed for evidence of boric acid leakage, to determine if the licensee properly applied applicable corrosion rates to the affected components; and properly assessed the effects of corrosion induced wastage on structural or pressure boundary integrity in accordance with the licensee procedures.
- Inservice Inspection Indication Evaluation Record for Code Case N-566-2 Compliance, Initiating Condition Report: 573530
- Inservice Inspection Indication Evaluation Record for Code Case N-566-2 Compliance, Initiating Condition Report: 573571 The inspectors reviewed the following condition reports (CRs) and associated corrective actions related to evidence of boric acid leakage, to evaluate if the corrective actions completed were consistent with the requirements of the ASME Code and 10 CFR Part 50, Appendix B, Criterion XVI.
CR 568076, Boric Acid Discovered at 1-IC-26 CR 568077, Boric Acid Discovered at 1-IC-1 CR 568078, Boric Acid Discovered at 1-IC-4 CR 568080, Boric Acid Discovered at 1-RC-1053 CR 568082, Boric Acid Discovered at 1-RC-1057 CR 568083, Boric Acid Discovered at Union Associated with 1-RC-RV-1 CR 568084, Boric Acid Discovered at 1-CH-332 CR 568107, Boric Acid Leakage Discovered at 1-SS-TV-109B CR 568109, Boric Acid Leakage Discovered at 1-RC-69 CR 568119, Boric Acid Leakage Discovered at 1-CH-360 CR 568121, Boric Acid Leakage Discovered at Various Components CR 568125, Boric Acid Leakage Discovered at Various Components Identification and Resolution of Problems The inspectors reviewed a sample of ISI-related issues entered into the CAP to determine if the licensee had appropriately described the scope of the problem, and had initiated corrective actions. The review also included the licensees consideration and assessment of operating experience events applicable to the plant. The inspectors performed this review to ensure compliance with 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requirements.
b. Findings
No findings were identified.
1R11 Licensed Operator Requalification Program and Licensed Operator Performance
.1 Resident Inspector Quarterly Review
a. Inspection Scope
The inspectors reviewed a licensed operator performance on January 14, 2015, during a simulator scenario which involved a steam generator tube rupture and an emergency boration for a reactor failing to trip. The scenario required classifications and notifications that were counted for NRC performance indicator input.
The inspectors observed the following elements of crew performance in terms of communications:
- (1) ability to take timely and proper actions;
- (2) prioritizing, interpreting, and verifying alarms;
- (3) correct use and implementation of procedures, including the alarm response procedures;
- (4) timely control board operation and manipulation, including high-risk operator actions; and,
- (5) oversight and direction provided by the shift supervisor, including the ability to identify and implement appropriate TS actions. The inspectors observed the post training critique to determine that weaknesses or improvement areas revealed by the training were captured by the instructor and reviewed with the operators. Documents reviewed are listed in the Attachment to this report.
b. Findings
No findings were identified.
.2 Quarterly Control Room Operator Performance Observations
a. Inspection Scope
During the inspection period, the inspectors conducted four observations of licensed reactor operators actions and activities to ensure that the activities were consistent with the licensee procedures and regulatory requirements. These observations took place during both normal and off-normal plant working hours. As part of this assessment, the inspectors observed the following elements of operator performance:
- (1) operator compliance and use of plant procedures including technical specifications;
- (2) control board/in-plant component manipulations;
- (3) use and interpretation of plant instruments, indicators and alarms;
- (4) documentation of activities;
- (5) management and supervision of activities; and,
- (6) communication between crew members.
The inspectors observed and assessed licensed operator performance during the following events:
- During 2J EDG Surveillance on February 10, 2015
- On March 26, 2015 during Unit 1 startup activities, from Mode 4 to Mode 3
- On March 27, 2015 during Unit 1 startup activities from Mode 3 to Mode 2
b. Findings
No findings were identified.
1R12 Maintenance Effectiveness
a. Inspection Scope
For the three equipment issues listed below, the inspectors evaluated the effectiveness of the respective licensee's preventive and corrective maintenance. The inspectors performed walkdowns of the accessible portions of the systems, performed in-office reviews of procedures and evaluations, and held discussions with licensee staff. The inspectors compared the licensees actions with the requirements of the Maintenance Rule (10 CFR 50.65), and licensee procedure ER-AA-MRL-10, Maintenance Rule Program, Revision 6. Other documents reviewed are listed in the Attachment to this report.
- CR568982, Drive gear broken on 1-SW-230
- CR568951, Hydro Test Pump speed control constant at varying outputs
- CR567185, Two channels of U1 RWST level removed from service during calibrations
b. Findings
Introduction:
A Green self-revealing NCV of 10 CFR 50 Appendix B, Criterion V, Instructions, Procedures, and Drawings, was identified for the licensees failure to follow work management procedures. Specifically, the licensee failed to follow the conduct of maintenance procedure, MM-AA-100, Conduct of Maintenance, Revision 10, where maintenance personnel should use an assortment of techniques and tools to avoid errors during work execution. Attachment 6 step 1b outlines various human error prevention techniques that should have been used during the work execution including self checking and questioning attitude.
Description:
On December 10, 2014, the licensee was performing planned level transmitter calibrations for Level Channel I instrument loop (1-QS-L-100C) and Channel II instrument loop (1-QS-L-100D), for Unit 1 Refueling Water Storage Tank (RWST).
The RWST is the suction source for all Emergency Core Cooling System pumps during the injection phase of a LOCA. There are three RWST level channels that feed the logic for auto-starting the Recirculation Spray (RS) system. The RS system is designed to lower containment pressure for a loss of coolant accident (LOCA) by spraying water from the sumps in containment back into the containment atmosphere. As an event progresses, the RWST level will decrease, and water collects in the containment sumps.
The RS system is initiated with the receipt of Containment Pressure High-High signal coincident with RWST Level-Low. With Containment Pressure High-High, and two of the three RWST level channels indicate RWST level low, the actuation logic to auto-start the RS system is satisfied.
TS 3.3.2, condition D, allows one RWST level channel to be inoperable at any time.
During maintenance or surveillance activities, to satisfy TS 3.3.2, condition D, only one level channel is placed in trip for calibration at a time. However, on December 10, 2014, two required RWST level channels were inadvertently made inoperable due to concurrent channel level calibration work. The channel calibration work was briefed with emphasis to remove one level transmitter at a time; however there was no discussion about which channel calibration would be performed first: 1-QS-L-100C or 1-QS-L-100D.
Due to communication and coordination errors in the work control process, two work packages were worked simultaneously. The channel calibration work is conducted in two locations, the instrument rack and locally at the RWST. The technicians at the instrument rack proceeded to trip 1-QS-L-100D for calibration, per the TS3.3.2 condition D action. The technicians at the RWST proceeded to isolate and drain the second channel, 1-QS-L-100C, for calibration, resulting in a low level indication for another tripped channel. Because of the condition of two inoperable RWST level channels, the station no longer met the requirements of TS 3.3.2 and had to enter TS 3.0.3 because TS 3.3.2 does not contain an action for two inoperable RWST level channels.
Additionally, the station entered TS 3.6.7, condition F, for three or more RS subsystems inoperable. The required action for TS 3.6.7, condition F, is to enter LCO 3.0.3. The RS system is comprised of four subsystems, and the pump suction source is the sumps in containment. All four RS subsystems were inoperable because part of the actuation logic to auto-start the system was satisfied due to two tripped RWST level channels, meaning the RS system would actuate immediately on Containment Pressure High-High. In the condition described, the RWST level-low did not mean that the RWST water was in the sumps. The RS suction source was severely reduced. Therefore, if the RS system was actuated on a Containment Pressure High-High indication, the RS subsystem pumps would auto-start and there would not be sufficient water for pump suction. The RS pumps would operate with reduced suction source until manually turned off by the operators, and therefore, all four RS subsystems were inoperable.
The inspectors reviewed Procedure MM-AA-100 Conduct of Maintenance, Revision 10, which provided the requirements for the conduct of maintenance process. Attachment 6 step 1b outlines various human error prevention techniques that should have been used during the work execution including self checking and questioning attitude. The inspectors concluded that the maintenance personnel did not use human error prevention tools when performing the maintenance.
Analysis:
The licensees failure to follow the conduct of maintenance procedure, MM-AA-100, Conduct of Maintenance, Revision 10, was a performance deficiency.
Specifically, on December 10, 2014, maintenance personnel failed to effectively use human error prevention tools when performing the maintenance on the RWST level channels which resulted in a loss of the safety function of the RS system. The performance deficiency was more than minor because it was associated with the configuration control attribute of the Barrier Integrity cornerstone and adversely affected the cornerstone objective to ensure that the physical design barriers (fuel cladding, reactor coolant system, and containment) protect the public from radionuclide releases caused by accidents or events and is therefore a finding. Specifically, the RS system safety function was inadvertently rendered inoperable. The inspectors performed a Phase 1 analysis using the IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 3 Barrier Integrity Screening Questions, dated June 19, 2012, and Appendix H Containment Integrity Significance Determination Process, dated May 6, 2004, and determined the finding required a detailed risk evaluation because it involved the loss of safety function of the RS system.
A detailed risk evaluation was performed in accordance with NRC Inspection Manual Chapter (IMC) 0609, Appendix A by a regional senior reactor analyst using the latest NRC North Anna SPAR model and Saphire risk program. The major analysis assumptions included: a thirty-two minute exposure interval, and a non-recoverable loss of both inside recirculation spray pumps and both outside recirculation pumps. The dominant risk sequence was a small break loss of coolant accident initiator, success of the reactor protection system, success of feedwater, success of high pressure injection, success of secondary side cooldown and failure of recirculation spray resulting in loss of core and containment heat removal capability. The risk was mitigated by the short exposure period. The risk evaluation result was an increase in core damage frequency of <1 E-6/year and an increase in large early release fraction of <1 E -7/year, a GREEN finding of very low safety significance.
The finding has a cross-cutting aspect in the area of human performance associated with the work management attribute because the organization failed to implement a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority. Furthermore, the licensee work process control includes the identification and management of risk commensurate to the work and the need for coordination with different groups or job activities. Specifically, due to poor communication and coordination between the Control Room and the technicians calibrating the RWST level channels, and amongst the team of technicians calibrating the RWST level transmitters, the RS system was inoperable [H.5].
Enforcement:
Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, required, in part, that activities affecting quality be prescribed by documented instructions and procedures appropriate to the circumstances and shall be accomplished in accordance with these instructions and procedures.
The licensees maintenance procedure, MM-AA-100, Conduct of Maintenance, Revision 10, requires maintenance personnel to use an assortment of techniques and tools to avoid errors during work execution. Attachment 6 step 1b outlines various human error prevention techniques that should have been used during the work execution including self checking and questioning attitude.
Contrary to this requirement, the licensee failed to manage and accomplish activities affecting quality in accordance with documented procedures. Specifically, on December 10, 2014, maintenance personnel did not use human error prevention tools when performing the maintenance on the RWST level channels which resulted in the loss of the safety function of the RS system. Because it is of very low safety significance (Green), this violation is being treated as an NCV, consistent with Section 2.3.2.a of the NRC Enforcement Policy. The violation was entered into the licensees corrective action program as CR 567185. This non-cited violation is identified as NCV 05000338/2015001-01, Failure To Follow Procedure For RWST Instruments.
1R13 Maintenance Risk Assessments and Emergent Work Control
a. Inspection Scope
The inspectors evaluated, as appropriate, the six activities listed below for the following:
- (1) effectiveness of the risk assessments performed before maintenance activities were conducted;
- (2) management of risk;
- (3) appropriate and necessary steps taken to plan and control the resulting emergent work activities upon identification of an unforeseen situation; and,
- (4) adequate identification and resolution of maintenance risk assessments and emergent work problems. The inspectors verified that the licensee was in compliance with the requirements of 10 CFR 50.65 (a)(4) and the data output from the licensees safety monitor associated with the risk profile of Units 1 and 2. The inspectors reviewed the corrective action program to verify that deficiencies in risk assessments were being identified and properly resolved.
- Emergent work for Unit 1 A Component Cooling Heat Exchange valve failure on January 11, 2015
- Outage safety review for Unit 1 forced outage on B main feed regulating valve operation on February 26, 2015
- Emergent work on Unit 2 C containment air recirculation fan
- Maintenance activities during transition from Mode 4 to Mode 3 on March 25, 2015
- Maintenance activities during transition from Mode 3 to Mode 2 on March 26, 2015
- Maintenance activities during transition from Mode 2 to Mode 1 on March 27, 2015
b. Findings
No findings were identified.
1R15 Operability Determinations and Functionality Assessments
.1 Operability and Functionality Review
a. Inspection Scope
The inspectors reviewed five operability determinations and functionality assessments, listed below, affecting risk-significant mitigating systems, to assess, as appropriate: (1)the technical adequacy of the evaluations;
- (2) whether continued system operability was warranted;
- (3) whether other existing degraded conditions were considered as compensatory measures;
- (4) whether the compensatory measures, if involved, were in place, would work as intended, and were appropriately controlled; and,
- (5) where continued operability was considered unjustified, the impact on TS Limiting Conditions for Operation and the risk significance in accordance with the Significant Determination Process (SDP). The inspectors review included a verification that operability determinations (OD) were made as specified by procedure OP-AA-102, Operability Determination, Revision 12. Other documents reviewed are listed in the Attachment to this report.
- Review of OD000604 Revision 2, Unit 2 Control Rod E-11 rod position indication signal stability
- Review of OD000605, OD to Evaluate N2 Leakage from 2-GN-TK-1B
- Review of OD000609, Need to Determine Operability of C RCS Loop with Flawed Elbow
- Review of OD000612, AFW Check Valve Leakage (2-FW-70 & 2-FW-279)
b. Findings
No findings were identified.
.2 Operator Workaround (OWA) Management
a. Inspection Scope
The inspectors performed a review regarding the licensees assessments and corrective actions for OWAs. The inspectors reviewed the cumulative effects of the licensees OWAs and procedure OP-AA-1700, Revision 6, Operations Aggregate Impact. The inspectors reviewed the data package associated with this procedure which included an evaluation of the cumulative effects of the OWAs on the operators ability to safely operate the plant and effectively respond to abnormal and emergency plant conditions.
The inspectors reviewed and monitored licensee planned and completed corrective actions to address underlying equipment issues causing the OWAs. The inspectors also evaluated OWAs against the requirements of the licensees corrective action program as specified in PI-AA-200, Corrective Action, Revision 23, 10 CFR 50, Appendix B, and OP-AA-100, "Conduct of Operations," Revision 27.
b. Findings and Observations
No findings were identified.
In general, the inspectors verified that the licensee has identified OWA problems at an appropriate threshold and entered them in the corrective action program, and has proposed or implemented appropriate corrective actions.
1R18 Plant Modifications
Permanent Modifications
a. Inspection Scope
The inspectors reviewed the four completed permanent plant modification design change packages (DCP) listed below. The inspectors conducted a walkdown of the installation, discussed the desired improvement with system engineers, and reviewed the 10 CFR 50.59, Safety Review/Regulatory Screening, technical drawings, test plans and the modification package to assess the TS implications. Other documents reviewed are listed in the Attachment to this report.
- DC-NA-14-00004, Install Tornado Missile Protection at U1/U2 AFW Pipe Tunnels.
b. Findings
No findings were identified.
1R19 Post Maintenance Testing
a. Inspection Scope
The inspectors reviewed six post-maintenance test procedures and/or test activities, listed below, for selected risk-significant mitigating systems to assess whether:
- (1) the effect of testing on the plant had been adequately addressed by control room and/or engineering personnel;
- (2) testing was adequate for the maintenance performed; (3)acceptance criteria were clear and adequately demonstrated operational readiness consistent with design and licensing basis documents;
- (4) test instrumentation had current calibrations, range, and accuracy consistent with the application;
- (5) tests were performed as written with applicable prerequisites satisfied;
- (6) jumpers installed or leads lifted were properly controlled;
- (7) test equipment was removed following testing; and,
- (8) equipment was returned to the status required to perform in accordance with VPAP-2003, Post Maintenance Testing Program, Revision 14.
- WO59102815326, Valve Gearbox Replacement for 1A Component Cooling HX Service Water (SW) Return No. 4
- WO59102400280, Pump Repair for Hydro Test Pump 1-SI-P-2
- WO59102813915, AMSAC Controller Module Replacement
- WO59102813478, 01-FW-FCV-1498 Repair Positioner
- 1-PT-83.12J, 1J Diesel Generator Test (Start by ESF Actuation) Followed by 24-Hour Run and Hot Restart Test
- WO59102832388/WO59102763186, 1-FW-P-2, Turbine Driven Auxiliary Feedwater Pump and Valve Test
b. Findings
No findings were identified.
1R20 Refueling and Other Outage Activities
.1 Unit 1 Refueling Outage
a. Inspection Scope
The inspectors reviewed the Outage Safety Review (OSR) and contingency plans for the Unit 1 refueling outage, which began March 7, 2015, to confirm that the licensee had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing a plan that assured maintenance of defense-in-depth. The inspectors also confirmed that the licensee had mitigation/response strategies in place for any losses of key safety functions. Using NRC inspection procedure 71111.20, Refueling and Outage Activities, the inspectors observed portions of the refueling, and maintenance activities to verify that the licensee maintained defense-in-depth commensurate with the outage risk plan and applicable TS. The inspectors monitored licensee controls over the outage activities listed below.
- Licensee configuration management, including daily outage reports, to evaluate maintenance of defense-in-depth commensurate with the OSR for key safety functions and compliance with the applicable TS when taking equipment out of service.
- Implementation of clearance activities and confirmation that tags were properly hung and equipment appropriately configured to safely support the work or testing.
- Installation and configuration of Reactor Coolant System instrumentation for system pressure, level, and temperature to provide accurate indication, and an accounting for instrument error.
- Implementation of licensee procedures for foreign material exclusion.
- Controls over the status and configuration of electrical systems to ensure that TS and outage safety plan requirements were met, and controls over switchyard activities.
- Controls to ensure that outage work was not impacting the ability of the operators to operate the spent fuel pool cooling system.
- Reactor inventory controls including flow paths, configurations, and alternative means for inventory addition, and controls to prevent inventory loss.
- Controls over activities and structure, system or component (SSCs) which could affect reactivity.
- Fatigue management in accordance with meeting the rule requirements for each process.
- Refueling activities, including fuel handling operations (inspection, sipping, reconstitution and insertion), and fuel assemblies tracking, including new fuel, from core offload through core reload.
- Controls over containment penetrations, per TS, such that containment closure could be achieved at all times.
- Licensee identification and resolution of problems related to refueling outage activities
- Startup and ascension to full power operation, tracking of startup prerequisites, walkdown of the containment to verify that debris had not been left which could block emergency core cooling system strainers, and the review of reactor physics testing.
b. Findings
No findings were identified.
.2 Unit 1 Forced Outage for RCS Pressure Boundary Leak
a. Inspection Scope
Unit 1 forced outage on December 22, 2014, due to a leak in an RCS drain pipe, which continued until January 1, 2015. During the forced outage period, the inspectors used NRC inspection procedure 71111.20, Refueling and Outage Activities, to observe portions of the maintenance and startup activities to verify that the licensee maintained defense-in-depth commensurate with outage risk assessments and applicable TS. The inspectors reviewed licensee actions for the outage activities listed below.
- Licensee configuration management, including daily outage reports, to evaluate defense-in-depth commensurate with the outage safety plan and compliance with the applicable TS when taking equipment out of service.
- Controls over the status and configuration of electrical systems and switchyard to ensure that TS and outage safety plan requirements were met.
- Decay heat removal processes to verify proper operation and that steam generators, when relied upon, were a viable means of backup cooling.
- Containment closure activities, including a focused containment walkdown prior to startup, to verify that there was no evidence of leakage and that debris had not been left which could affect the performance of the containment sump.
- Heat up and startup activities to verify TS, license conditions, and other requirements, commitments, and administrative procedure prerequisites for mode changes were met prior to changing modes or plant conditions. Reactor Coolant System (RCS) integrity was verified by reviewing RCS leakage calculations and containment integrity was verified by reviewing the status of containment penetrations and containment isolation valves.
b. Findings
No findings were identified.
.3 Unit 1 Forced Outage for Circuit Card Failure
a. Inspection Scope
Unit 1 forced outage on February 26, 2015, due to failed circuit card for the B main feed regulator valve that went closed. During the forced outage period, the inspectors used NRC inspection procedure 71111.20, Refueling and Outage Activities, to observe portions of the maintenance and startup activities to verify that the licensee maintained defense-in-depth commensurate with outage risk assessments and applicable TS. The inspectors reviewed licensee actions for the outage activities listed below.
- Licensee configuration management, including daily outage reports, to evaluate defense-in-depth commensurate with the outage safety plan and compliance with the applicable TS when taking equipment out of service.
- Controls over the status and configuration of electrical systems and switchyard to ensure that TS and outage safety plan requirements were met.
- Decay heat removal processes to verify proper operation and that steam generators, when relied upon, were a viable means of backup cooling.
- Containment closure activities, including a focused containment walkdown prior to startup, to verify that there was no evidence of leakage and that debris had not been left which could affect the performance of the containment sump.
- Heat up and startup activities to verify TS, license conditions, and other requirements, commitments, and administrative procedure prerequisites for mode changes were met prior to changing modes or plant conditions. Reactor Coolant System (RCS) integrity was verified by reviewing RCS leakage calculations and containment integrity was verified by reviewing the status of containment penetrations and containment isolation valves.
b. Findings
No findings were identified.
1R22 Surveillance Testing
a. Inspection Scope
For the seven surveillance tests listed below, the inspectors examined the test procedures, witnessed testing, or reviewed test records and data packages, to determine whether the scope of testing adequately demonstrated that the affected equipment was functional and operable, and that the surveillance requirements of TS were met. The inspectors also determined whether the testing effectively demonstrated that the systems or components were operationally ready and capable of performing their intended safety functions.
In-Service Test:
- 1-PT-75.2A, Service Water Pump (1-SW-P-1A) Quarterly Test, Revision 55
- 2-PT-57.1B, Emergency Core Cooling Subsystem - Low Head Safety Injection Pump (2-SI-P-1B), Revision 60 RCS Leakage:
- 1-GOP-52.2A, Identifying Increased RCS Leakage, Revision 1 Containment Isolation Valve:
- 1-PT-57.5A, Leakrate Test of 1-SI-P-1A and 1-SI-4, Revision 23
- 1-PT-57.5B, Leakrate Test of 1-SI-P-1B and 1-SI-21, Revision 25 Other Surveillance Tests:
- 1-PT-14.1, Charging Pump 1-CH-P-1A, Revision 54
- 2-PT-82J, 2J Emergency Diesel Generator Slow Start Test, Revision 57
b. Findings
No findings were identified.
1EP6 Drill Evaluation Emergency Preparedness (EP) Drill
a. Inspection Scope
On January 14, 2015, the inspectors reviewed and observed the performance of a drill that involved a Site Area Emergency where an automatic trip failed to shutdown the reactor and a faulted steam generator. The inspectors assessed emergency procedure usage, emergency plan classification, notifications, and the licensees identification and entrance of any problems into their corrective action program. This inspection evaluated the adequacy of the licensees conduct of the drill and performance critique. Exercise issues were captured by the licensee in their corrective action program as CRs.
Requalification training deficiencies were captured within the operator training program.
b. Findings
No findings were identified.
RADIATION SAFETY
Cornerstones: Public Radiation Safety and Occupational Radiation Safety
2RS1 Radiological Hazard Assessment and Exposure Controls
a. Inspection Scope
Hazard Assessment and Instructions to Workers The inspectors discussed the possibility of changes to plant operations that could contribute to significant new radiological conditions since the last inspection with. The inspectors independently measured radiation dose rates or directly observed conduct of licensee radiation surveys for selected radiologically controlled areas (RCAs) during plant walkdowns. The inspectors reviewed survey records for several plant areas in the auxiliary building, rad waste processing and Independent Spent Fuel Storage Installation (ISFSI), including surveys for alpha emitters, airborne radioactivity, gamma surveys with a range of dose rate gradients, and pre-job and some post-job surveys for tasks. During facility tours, the inspectors directly observed labeling of radioactive material and postings for radiation areas, high radiation areas (HRAs) within the RCA of the auxiliary building and radioactive waste (radwaste) processing and storage locations. The inspectors reviewed radiation work permit (RWP) details to assess communication of radiological control requirements and current radiological conditions to workers for select jobs in HRAs. The inspector observed the oversight and coaching of workers in the containment exit undress area.
Control of Radioactive Material The inspectors observed surveys of material and personnel being released from the RCA using small article monitor, personnel contamination monitor, and portal monitor instruments, in accordance with procedures.
Inspectors also observed instrument calibration stickers and observed and discussed setpoints for some instrumentation. The inspectors reviewed records of inventory selected sealed sources and discussed nationally tracked source transactions with licensee staff.
Risk-Significant Radiation Areas, Hazard Control and Work Practices The inspectors evaluated access barrier effectiveness for selected Locked High Radiation Area (LHRA)locations and discussed procedural guidance and adherence for LHRA and Very High Radiation Area (VHRA) controls with health physics (HP) supervisors. The inspectors observed and evaluated controls for the storage of irradiated material within the spent fuel pool (SFP). Established radiological controls (including airborne controls) were evaluated for outage related work on Unit 1. In addition, the inspectors reviewed and discussed licensee controls for areas where dose rates could change significantly.
Through direct observations and interviews with licensee staff, the inspectors evaluated occupational workers adherence to selected RWPs and Health Physics Technicians (HPTs) proficiency in providing job coverage. Electronic dosimeter (ED) alarm set points and worker stay times were evaluated against area radiation survey results for selected entries into various high radiation areas and locked high radiation areas. The inspectors discussed the use of personnel dosimetry for multibadging work and areas with high dose gradients. The inspectors also evaluated worker response to dose and dose rate alarms during selected work activities. Inspectors reviewed RWPs for airborne radioactivity areas.
Problem Identification and Resolution The inspectors reviewed and assessed Condition Reports (CRs) associated with radiological hazard assessment and control. The inspectors evaluated the licensees ability to identify and resolve the issues in accordance with licensee procedures. The inspectors also reviewed recent self-assessment results.
Radiation protection activities were evaluated against the requirements of Updated Final Safety Analysis Report (UFSAR) Section 12; Technical Specifications (TS) Sections 5.4 (Procedures) and 5.7 (High Radiation Areas); 10 CFR Parts 19 and 20; and approved licensee procedures. Licensee programs for monitoring materials and personnel released from the RCA were evaluated against 10 CFR Part 20 and IE Circular 81-07, Control of Radioactively Contaminated Material. Documents reviewed are listed in the report Attachment.
b. Findings
No findings were identified.
OTHER ACTIVITIES
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity
4OA1 Performance Indicator (PI) Verification
a. Inspection Scope
The inspectors performed a periodic review of the three Unit 1 and 2 PIs listed below to assess the accuracy and completeness of the submitted data and whether the performance indicators were calculated in accordance with the guidance contained in Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7. The inspection was conducted in accordance with NRC inspection procedure 71151, Performance Indicator Verification. Specifically, the inspectors reviewed the Unit 1 and Unit 2 data reported to the NRC for the period January 1, 2014 through December 31, 2014. Documents reviewed included applicable NRC inspection reports, licensee event reports, operator logs, station performance indicators, and related CRs.
- Unplanned Scrams per 7000 Critical Hours (IE01)
- Unplanned Transients per 7000 Critical Hours(IE03)
- Unplanned Scrams With Complications (IE04)
b. Findings
No findings were identified.
4OA2 Problem Identification and Resolution
.1 Review of Items Entered into the Corrective Action Program
As required by NRC inspection procedure 71152, Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensees CAP. This review was accomplished by reviewing daily CR report summaries and periodically attending daily CR Review Team meetings.
.2 Annual Sample: Review of CR568624, The normal level controller for Unit 2 1A
feedwater heater has failed
a. Inspection Scope
The inspectors performed a review regarding the licensees assessments and corrective actions for CR568624, The normal level controller for Unit 2 1A feedwater heater has failed, to ensure that the full extent of the issue was identified, an appropriate evaluation was performed, and appropriate corrective actions were specified and prioritized. The inspectors also evaluated the CR against the requirements of the licensees CAP as specified in licensee procedure, PI-AA-200, Corrective Action Program, Revision 23 and 10 CFR 50, Appendix B.
b. Findings and Observations
No findings were identified. In general, the inspectors verified that the licensee had identified problems at an appropriate threshold and entered them into the CAP database, and had proposed or implemented appropriate corrective actions.
.3 Annual Sample: Review of CR567185, Two channels of U1 RWST level removed from
service during calibrations, and CR567188, North Anna Unit 1 Entered TS 3.0.3 due to 2 inoperable RWST Level Transmitters
a. Inspection Scope
The inspectors performed a review regarding the licensees assessments and corrective actions for CR567185, Two channels of U1 RWST level removed from service during calibrations, and CR567188, North Anna Unit 1 Entered TS 3.0.3 due to 2 inoperable RWST Level Transmitters, to ensure that the full extent of the issue was identified, an appropriate evaluation was performed, and appropriate corrective actions were specified and prioritized. The inspectors also evaluated the CR against the requirements of the licensees CAP as specified in licensee procedure, PI-AA-200, Corrective Action Program, Revision 23, and 10 CFR 50, Appendix B.
b. Findings and Observations
In general, the inspectors verified that the licensee had identified problems at an appropriate threshold and entered them into the CAP database, and had proposed or implemented appropriate corrective actions. See Section 1R12 for details of finding.
.4 Annual Sample: Review of CR568497, 3CND-P3 Oil bubbler low at 1/16th full
a. Inspection Scope
The inspectors performed a review regarding the licensees assessments and corrective actions for CR568497, 3CND-P3 Oil bubbler low at 1/16th full, to ensure that the full extent of the issue was identified, an appropriate evaluation was performed, and appropriate corrective actions were specified and prioritized. The inspectors also evaluated the CR against the requirements of the licensees CAP as specified in licensee procedure, PI-AA-200, Corrective Action Program, Revision 23, and 10 CFR 50, Appendix B.
b. Findings and Observations
No findings were identified. In general, the inspectors verified that the licensee had identified problems at an appropriate threshold and entered them into the CAP database, and had proposed or implemented appropriate corrective actions.
4OA3 Event Followup
.1 Unit 2 Feedwater Transient due to 4A Feedwater Heater Down Power
The inspectors followed up on actions taken in response to the failure of the Unit 2 4A Feedwater (FW) Heater Controller which caused a unit transient on January 4, 2015.
The 1A FW Heater Normal Level Controller failed and the normal level control/cascade valve for Unit 2 1A FW Heater failed closed and was unable to be adjusted. The licensee commenced ramp down for the unit to maintain reactor power. The inspectors reviewed the problem resolution documents and the licensee actions taken to ensure appropriate corrective actions were specified and prioritized. Documents reviewed are listed in the Attachment to this report.
.2 (Closed) LER 05000338/2014-002-00: Inadvertent Loss of Vital Instrumentation During
Maintenance Due to Personnel Error On December 10, 2014, with Unit 1 in Mode 1 at 100 percent power, Station technicians commenced scheduled periodic channel calibrations of level transmitters for the Unit 1 Refueling Water Storage Tank Level Channel I instrument loop and Channel II instrument loop. At 1344 hours0.0156 days <br />0.373 hours <br />0.00222 weeks <br />5.11392e-4 months <br />, two channels of the Unit 1 Refueling Water Storage Tank (RWST) level instrumentation were inadvertently removed from service at the same time during maintenance. Operations personnel responded by entering abnormal procedure 1-AP-3, Loss of Vital Instrumentation. The licensee also entered TS 3.0.3 due to two channels being inoperable that affect Recirculation Spray (RS) pump auto-start logic. At 1356 hours0.0157 days <br />0.377 hours <br />0.00224 weeks <br />5.15958e-4 months <br />, both level indications returned to normal. At 1417 hours0.0164 days <br />0.394 hours <br />0.00234 weeks <br />5.391685e-4 months <br />, Channel II was declared operable and TS 3.0.3 was cleared. At 1439, Channel I was declared operable and TS actions were cleared.
Had a containment depressurization actuation (CDA) occurred during this time, accident mitigation may have been impacted. The RS pumps would have started without sufficient suction water, however the control room could promptly reset the CDA signal and manually shutdown the RS pumps to prevent damage. The event posed no significant safety implications and the health and safety of the public were not affected by this event.
The cause of the event was personnel error. Station technicians failed to assess risk associated with the RWST level calibration tasks. Inattention as a result of repetition and/or becoming complacent and overconfident with the job task caused the team not to use human performance tools to mitigate the errors. Completed interim actions included removing the qualifications of the individuals involved until remediation was conducted; performing a stand down to ensure lessons learned are integrated into the daily work activities and department standards and expectations were reinforced; and supervisors have increased oversight for pre-job briefs and are maintaining field presence to ensure high rick error likely tasks are briefed adequately, barriers and defenses used and standards and expectations reinforced.
This issue is in the licensees CAP as CR567185, Two channels of U1 RWST level removed from service during maintenance. See Section 1R12 for details of finding.
4OA6 Meetings, Including Exit
Exit Meeting Summary
On April 22, 2015, the resident inspectors presented the inspection results to Mr. G.
Bischof and other members of the staff, who acknowledged the findings. The inspectors verified no proprietary information was retained by the inspectors or documented in this report.
ATTACHMENT: SUPPPLEMENTARY INFORMATION
SUPPLEMENTARY INFORMATION
KEY POINTS OF CONTACT
Licensee personnel
- M. Becker, Manager, Nuclear Outage and Planning
- G. Bischof, Site Vice President
- B. Derreberry, ISI/NDE Supervisor
- B. Evans, Manager Radiation Protection
- B. Gaspar, Manager, Nuclear Site Services
- R. Hanson, Manager, Nuclear Protection Services
- E. Hendrixson, Director, Nuclear Site Engineering
- L. Hilbert, Director, Nuclear Station Safety & Licensing
- J. Jenkins, Manager, Nuclear Maintenance
- P. Kemp, Supervisor, Station Licensing
- H. Le, Engineering Programs Manager,
- J. Leberstien, Technical Advisor, Licensing
- A. Maly, Supervisor Technical Services
- F. Mladen, Plant Manager
- N. Nicholson, Health Physicist III
- T. Pastor, Supervisor Radiation Protection Technical Services
- J. Plossl, Supervisor, Nuclear Station Procedures
- M. Sartain, Nuclear Engineering Vice President
- J. Schleser, Manager, Nuclear Organizational Effectiveness
- R. Simmons, Supervisor Radiation Protection Operations
- J. Slattery, Manager, Nuclear Operations
- W. Standley, Manager, Nuclear Training
- J. Swenson, Site Welding Engineer
- M. Whalen, Technical Advisor, Licensing
LIST OF ITEMS
OPENED, CLOSED AND DISCUSSED
Opened and Closed
- 05000338/2015001-01 NCV Failure To Follow Procedure For RWST Instruments (Section 1R12)
Closed
- 05000338/2014-002-00 LER Inadvertent Loss of Vital Instrumentation During Maintenance Due to Personnel Error (Section 4OA3.2)
Discussed
None