ML16314C026: Difference between revisions

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| number = ML16314C026
| number = ML16314C026
| issue date = 11/08/2016
| issue date = 11/08/2016
| title = Comanche Peak Nuclear Power Plant - NRC Integrated Inspection Report 05000445/2016003 and 05000446/2016003
| title = NRC Integrated Inspection Report 05000445/2016003 and 05000446/2016003
| author name = Groom J R
| author name = Groom J
| author affiliation = NRC/RGN-IV/DRP/RPB-A
| author affiliation = NRC/RGN-IV/DRP/RPB-A
| addressee name = Peters K
| addressee name = Peters K
Line 14: Line 14:
| page count = 29
| page count = 29
}}
}}
See also: [[followed by::IR 05000445/2016003]]
See also: [[see also::IR 05000445/2016003]]


=Text=
=Text=
{{#Wiki_filter:UNITED STATES
{{#Wiki_filter:UNITED STATES
NUCLEAR REGULATORY COMMISSION
                            NUCLEAR REGULATORY COMMISSION
REGION IV 1600 E. LAMAR BLVD.
                                                REGION IV
ARLINGTON, TX
                                          1600 E. LAMAR BLVD.
  76011-4511 November 8, 2016 Mr. Ken Peters, Senior Vice President
                                        ARLINGTON, TX 76011-4511
  and Chief Nuclear Officer
                                          November 8, 2016
TEX Operations Company LLC
Mr. Ken Peters, Senior Vice President
P.O. Box 1002
  and Chief Nuclear Officer
Glen Rose, TX 76043
TEX Operations Company LLC
SUBJECT: COMANCHE PEAK NUCLEAR POWER PLANT - NRC INTEGRATED INSPECTION REPORT 05000445/2016003
P.O. Box 1002
and 05000446/
Glen Rose, TX 76043
2016003 Dear Mr. Peters: On September 30, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Comanche Peak Nuclear Power Plant, Units 1 and 2. O n September 29 , 2016, the NRC inspectors discussed the results of this inspection
SUBJECT:       COMANCHE PEAK NUCLEAR POWER PLANT - NRC INTEGRATED
with Mr. S. Sewell , Senior Director of Engineering and Regulatory Affairs, and other members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report.
                INSPECTION REPORT 05000445/2016003 and 05000446/2016003
NRC inspectors documented two findings of very low safety significance (Green) in this report. All of these findings involved violations of NRC requirements.
Dear Mr. Peters:
If you contest the violations or significance of these NCVs, you should provide a response within  
On September 30, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an
30 days of the date of this inspection report, with the basis for your denial, to the U.S.
inspection at your Comanche Peak Nuclear Power Plant, Units 1 and 2. On September 29,
Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555
2016, the NRC inspectors discussed the results of this inspection with Mr. S. Sewell, Senior
-0001; and the NRC  
Director of Engineering and Regulatory Affairs, and other members of your staff. Inspectors
resident inspector at the Comanche Peak Nuclear Power Plant, Units 1 and 2. If you disagree with
documented the results of this inspection in the enclosed inspection report.
a cross-cutting aspect assignment
NRC inspectors documented two findings of very low safety significance (Green) in this report.
in this report, you should provide a response within 30
All of these findings involved violations of NRC requirements.
days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV; and the NRC  
If you contest the violations or significance of these NCVs, you should provide a response within
resident inspector at the Comanche Peak Nuclear Power Plant, Units 1 and 2. In accordance with Title 10 of the Code of Federal Regulations
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
(10 CFR) 2.390, "Public Inspections, Exemptions, Requests for Withholding,"
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with
a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC
copies to the Regional Administrator, Region IV; the Director, Office of Enforcement,
's Public Document Room or from the Publicly Available Records (PARS) component of the NRC's  
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC resident
K. Peters - 2 - Agencywide
inspector at the Comanche Peak Nuclear Power Plant, Units 1 and 2.
Documents Access and Management System (ADAMS).
If you disagree with a cross-cutting aspect assignment in this report, you should provide a
ADAMS is accessible from the NRC Web
response within 30 days of the date of this inspection report, with the basis for your
site at http://www.nrc.gov/reading
disagreement, to the Regional Administrator, Region IV; and the NRC resident inspector at the
-rm/adams.html
Comanche Peak Nuclear Power Plant, Units 1 and 2.
(the Public Electronic Reading Room).
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public
Sincerely, /RA/ Jeremy R. Groom, Branch Chief Project Branch A
Inspections, Exemptions, Requests for Withholding, a copy of this letter, its enclosure, and your
Division of Reactor Projects
response (if any) will be available electronically for public inspection in the NRCs Public
Docket Nos. 
Document Room or from the Publicly Available Records (PARS) component of the NRC's
50-445 and 50-446  License Nos. NPF-87 and NPF
-89 Enclosure: Inspection Report 05000445/2016003 and
    05000446/2016003
w/ Attachment:  Supplemental Information
cc w/ encl:  Electronic Distribution
 


  SUNSI Review
K. Peters                                    -2-
By:  JRG ADAMS  Yes    No  Non-Sensitive  Sensitive  Publicly Available
Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible
  Non-Publicly Available
from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic
Keyword: NRC-002 OFFICE SRI:DRP/A RI:DRP/A SPE:DRP/A BC:EB1 BC:EB2 BC:OB BC:PSB2 NAME JJosey RKumana RAlexander
Reading Room).
TFarnholtz
                                          Sincerely,
GWerner VGaddy HGepford SIGNATURE /RA/ /RA/ /RA/ /RA/ /RA/ /RA/ /RA/ DATE 10/21/16 10/24/16 10/19/16 10/19/16 10/25/16 10/20/16 10/20/16 OFFICE TL-IPAT BC:DRP/A NAME THipschman
                                          /RA/
  JGroom SIGNATURE /RA/ /RA/ DATE 10/19/16 11/8/16 
                                          Jeremy R. Groom, Branch Chief
  Letter to Ken Peters from Jeremy Groom dated November 8, 2016  SUBJECT: COMANCHE PEAK NUCLEAR POWER PLANT
                                          Project Branch A
-NRC INTEGRATED
                                          Division of Reactor Projects
         INSPECTION REPORT 05000445/201
Docket Nos. 50-445 and 50-446
6 00 3 and 05000446/201
License Nos. NPF-87 and NPF-89
6 00 3  DISTRIBUTION
Enclosure:
: Regional Administrator (Kriss.Kennedy@nrc.gov)
Inspection Report 05000445/2016003 and
Deputy Regional Administrator (Scott.Morris@nrc.gov) DRP Director (Troy.Pruett@nrc.gov)
  05000446/2016003
DRP Deputy Director (Ryan.Lantz@nrc.gov) DRS Director (Anton.Vegel@nrc.gov)
w/ Attachment: Supplemental Information
DRS Deputy Director (Jeff.Clark@nrc.gov)
cc w/ encl: Electronic Distribution
Senior Resident Inspector (Jeffrey.Josey@nrc.gov)
 
Resident Inspector (Rayomand.Kumana@nrc.gov)
 
Administrative Assistant (VACANT) Branch Chief, DRP/A (Jeremy.Groom@nrc.gov)
 
Senior Project Engineer, DRP/A (Ryan.Alexander@nrc.gov)
  SUNSI Review        ADAMS          Non-Sensitive  Publicly Available          Keyword:
Project Engineer, DRP/A (Thomas.Sullivan@nrc.gov)
  By: JRG                Yes No      Sensitive        Non-Publicly Available    NRC-002
Project Engineer, DRP/A (Mathew.Kirk@nrc.gov)
  OFFICE      SRI:DRP/A    RI:DRP/A  SPE:DRP/A    BC:EB1    BC:EB2        BC:OB      BC:PSB2
Public Affairs Officer (Victor.Dricks@nrc.gov)
  NAME         JJosey      RKumana    RAlexander    TFarnholtz GWerner        VGaddy      HGepford
Project Manager (Margaret.Watford@nrc.gov) Team Leader, DRS/IPAT (Thomas.Hipschman@nrc.gov) RITS Coordinator (Marisa.Herrera@nrc.gov)
  SIGNATURE /RA/            /RA/      /RA/          /RA/      /RA/          /RA/        /RA/
ACES (R4Enforcement.Resource@nrc.gov)
  DATE        10/21/16    10/24/16  10/19/16      10/19/16  10/25/16      10/20/16    10/20/16
Regional Counsel (Karla.Fuller@nrc.gov) Congressional Affairs Officer (Jenny.Weil@nrc.gov)
  OFFICE      TL-IPAT      BC:DRP/A
RIV Congressional Affairs Officer (Angel.Moreno@nrc.gov)
  NAME        THipschman JGroom
RIV/ETA: OEDO (Jeremy.Bowen@nrc.gov) ROPreports
  SIGNATURE /RA/            /RA/
  Electronic Distribution for Comanche Peak Nuclear Power Plant   
  DATE        10/19/16    11/8/16
  A-1 Attachment
                                     
U.S. NUCLEAR REGULATORY COMMISSION
Letter to Ken Peters from Jeremy Groom dated November 8, 2016
REGION IV Docket: 05000445, 05000446
SUBJECT: COMANCHE PEAK NUCLEAR POWER PLANT-NRC INTEGRATED
License: NPF-87, NPF-89 Report: 05000 445/20 16003 and 05000446/201600
            INSPECTION REPORT 05000445/2016003 and 05000446/2016003
3 Licensee: TEX Operations
DISTRIBUTION:
Company, LLC
Regional Administrator (Kriss.Kennedy@nrc.gov)
Facility: Comanche Peak Nuclear Power Plant, Units 1 and 2
Deputy Regional Administrator (Scott.Morris@nrc.gov)
Location: 6322 N. FM
DRP Director (Troy.Pruett@nrc.gov)
-56, Glen Rose, Texas
DRP Deputy Director (Ryan.Lantz@nrc.gov)
Dates: July 1 through September 30, 2016 Inspectors:
DRS Director (Anton.Vegel@nrc.gov)
J. Josey, Senior Resident Inspector
DRS Deputy Director (Jeff.Clark@nrc.gov)
R. Kumana, Resident Inspector
Senior Resident Inspector (Jeffrey.Josey@nrc.gov)
W. Cullum, Reactor Inspector
Resident Inspector (Rayomand.Kumana@nrc.gov)
Approved By: Jeremy R. Groom
Administrative Assistant (VACANT)
Chief, Project Branch
Branch Chief, DRP/A (Jeremy.Groom@nrc.gov)
A Division of Reactor Projects
Senior Project Engineer, DRP/A (Ryan.Alexander@nrc.gov)
   
Project Engineer, DRP/A (Thomas.Sullivan@nrc.gov)
  A-2 SUMMARY  IR 05000445/2016003 and 05000446/2016003
Project Engineer, DRP/A (Mathew.Kirk@nrc.gov)
; 07/01/2016 - 09/3 0/2016; Comanche
Public Affairs Officer (Victor.Dricks@nrc.gov)
Peak NPP, Units 1 and 2
Project Manager (Margaret.Watford@nrc.gov)
; Maintenance Effectiveness
Team Leader, DRS/IPAT (Thomas.Hipschman@nrc.gov)
, Problem Identification and Resolution
RITS Coordinator (Marisa.Herrera@nrc.gov)
  The inspection activities described in this report were performed between July 1, 2016, through September 30, 2016, by the resident inspectors at the Comanche Peak
ACES (R4Enforcement.Resource@nrc.gov)
Nuclear Power Plant
Regional Counsel (Karla.Fuller@nrc.gov)
and an inspector from the NRC's Region IV office. Two finding s of very low safety significance (Green) are documented in this report. Both of these finding s involved a violation of NRC requirements.  The significance of inspection findings is indicated by their color (Green, White,  
Congressional Affairs Officer (Jenny.Weil@nrc.gov)
Yellow, or Red), which is determined using Inspection Manual Chapter
RIV Congressional Affairs Officer (Angel.Moreno@nrc.gov)
0609, "Significance Determination Process."  Their cross
RIV/ETA: OEDO (Jeremy.Bowen@nrc.gov)
-cutting aspects are determined using Inspection
ROPreports
Manual Chapter 0310, "Aspects within
Electronic Distribution for Comanche Peak Nuclear Power Plant
the Cross-Cutting Areas."  Violations of NRC requirements are dispositioned in accordance with the NRC Enforcement Policy. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in  
 
NUREG-1649, "Reactor Oversight Process."
            U.S. NUCLEAR REGULATORY COMMISSION
  Cornerstone:  Initiating Events
                              REGION IV
  Green.  The inspectors identified a non
Docket:    05000445, 05000446
-cited violation of 10 CFR 50.65(a)(4), "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants," for
License:    NPF-87, NPF-89
the licensee's failure to adequately manage the increase in risk associated with the potential for a loss of decay heat removal during refueling outages.
Report:    05000445/2016003 and 05000446/2016003
Specifically, the licensee implemented a risk management action that did not reduce the risk
Licensee:  TEX Operations Company, LLC
, but instead called for placing a safety injection pump in service during periods where this action is prohibited by plant's technical specifications for low temperature over pressure protection.  The inspectors determined this was an ineffective risk management action because the use of a safety injection pump during low pressure and temperature conditions would place the plant in an unanalyzed condition, resulting in an increase in risk. As an immediate corrective action, the licensee initiated Condition Report CR
Facility:  Comanche Peak Nuclear Power Plant, Units 1 and 2
-2015-009109 to evaluate appropriate risk management actions. This finding was entered into the licensee's corrective action program as Condition
Location:  6322 N. FM-56, Glen Rose, Texas
Report CR-2015-009109.  
Dates:      July 1 through September 30, 2016
The failure to manage the increase in ris
Inspectors: J. Josey, Senior Resident Inspector
k associated with the potential for a loss of decay heat removal during refueling activities is a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the procedure quality attribute of the Initiating Events Cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Using Inspection Manual Chapte
            R. Kumana, Resident Inspector
r 0609, Appendix K, "Maintenance Risk Assessment and Risk Management Significance Determination Process," dated May 19, 2005, Flowchart 1, "Assessment of Risk Deficit," the inspectors determined the need to calculate the risk deficit to determine the significance of this issue.  A senior reactor analyst performed a bounding qualitative assessment and determined the incremental core damage probability deficit was less than 1E
            W. Cullum, Reactor Inspector
-6 and the incremental large early release probability deficit was less than 1E
Approved    Jeremy R. Groom
-7, based on the availability of additional equipment to mitigate the loss of decay heat removal.  In
    By:    Chief, Project Branch A
accordance with Flowchart 1 in Appendix K, because incremental core damage probability deficit was less than 1E
            Division of Reactor Projects
-6 and incremental large early release probability deficit was less than 1E-7, the finding screened as having very low safety significance (Green).
                                  A-1                        Attachment
  The finding has a human performance cross
 
-cutting aspect associated with bases for decisions, in that, the licensee failed to ensure that operations leadership adequately communicate potential 
                                              SUMMARY
  A-3 problems with the risk management action to start a safety injection pump when in a mode of applicability for low temperature over pressure protection [H.10].  (Section 4OA2)
IR 05000445/2016003 and 05000446/2016003; 07/01/2016 - 09/30/2016; Comanche Peak
  Cornerstone:  Mitigating Systems
NPP, Units 1 and 2; Maintenance Effectiveness, Problem Identification and Resolution
  Green.  The inspectors identified a non
The inspection activities described in this report were performed between July 1, 2016, through
-cited violation of 10 CFR 50.65(a)(2), "Requirements for monitoring the effectiveness of maintenance at nuclear power plants."  Specifically, the licensee failed to demonstrate that the performance of the Unit 2 auxiliary feedwater check valves was being effectively controlled through the performance of appropriate preventive maintenance. The licensee's failure to perform appropriate maintenance resulted in several failures of the check valves.  The licensee entered this issue into corrective action program as CR-2016-008312.  The licensee's failure to effectively monitor the performance of maintenance rule scoped
September 30, 2016, by the resident inspectors at the Comanche Peak Nuclear Power Plant
equipment in accordance with 10 CFR 50.65(a)(2) was a performance deficiency.  The performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment performance attribute of the Mitigating Systems Cornerstone
and an inspector from the NRCs Region IV office. Two findings of very low safety significance
and affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequencesSpecifically, the licensee failed to demonstrate that the performance of the Unit 2 auxiliary feedwater check valves was being effectively controlled through the performance of appropriate  
(Green) are documented in this report. Both of these findings involved a violation of NRC
preventive maintenance which resulted in failures of the valves. Using Inspection Manual Chapter (IMC) 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At
requirements. The significance of inspection findings is indicated by their color (Green, White,
-Power," dated June 19, 2012, inspectors determined that this finding was of very low safety significance (Green) because the finding (1) was not a deficiency affecting the design and qualification of a mitigating structure, system, or component, and did not result in a loss of operability or functionality, (2) did not represent a loss of system and/or function, (3) did not represent an actual loss of function of at least a single train for longer than its allowed outage time, or two separate safety systems out
Yellow, or Red), which is determined using Inspection Manual Chapter 0609, Significance
-of-service for longer than their technical specification allowed outage time, and (4) did not represent an actual loss of function of one or more non
Determination Process. Their cross-cutting aspects are determined using Inspection Manual
-technical specification trains of equipment designated as high safety-significant for greater than 24 hours in accordance with the licensee's maintenance rule program.  A cross-cutting aspect was not assigned to this finding because the performance deficiency occurred in 1996, and therefore, is not indicative of current licensee performance.  (Section 1R12)
Chapter 0310, Aspects within the Cross-Cutting Areas. Violations of NRC requirements are
  Licensee-Identified Violations
dispositioned in accordance with the NRC Enforcement Policy. The NRCs program for
  None    
overseeing the safe operation of commercial nuclear power reactors is described in
  A-4 PLANT STATUS
NUREG-1649, Reactor Oversight Process.
  Unit 1 and Unit 2 began the inspection period at approximately 100 percent power and operated at that power level for the entire inspection period.
Cornerstone: Initiating Events
  REPORT DETAILS
*  Green. The inspectors identified a non-cited violation of 10 CFR 50.65(a)(4), Requirements
  1. REACTOR SAFETY
    for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, for the licensees
  Cornerstones:  Initiating Events, Mitigating Systems, and Barrier Integrity
    failure to adequately manage the increase in risk associated with the potential for a loss of
  1 R 01 Adverse Weather Protection (71111.01)
    decay heat removal during refueling outages. Specifically, the licensee implemented a risk
.1 Summer Readiness for Offsite and Alternate
    management action that did not reduce the risk, but instead called for placing a safety
AC Power Systems a. Inspection Scope
    injection pump in service during periods where this action is prohibited by plants technical
On July 20, 2016, the inspectors completed an inspection of the station's off
    specifications for low temperature over pressure protection. The inspectors determined this
-site and alternate-ac power systems.
    was an ineffective risk management action because the use of a safety injection pump
The inspectors inspected the material condition of these systems, including transformers and other switchyard equipment
    during low pressure and temperature conditions would place the plant in an unanalyzed
to verify that plant features and procedures were appropriate for operation and continued availability of off
    condition, resulting in an increase in risk. As an immediate corrective action, the licensee
-site and alternate
    initiated Condition Report CR-2015-009109 to evaluate appropriate risk management
-ac power systems. The inspectors reviewed outstanding work orders and open condition reports for these systems
    actions. This finding was entered into the licensees corrective action program as Condition
.  The inspectors walked down the switchyard to observe the material condition of equipment providing off-site power sources. The inspectors verified that the licensee's procedures included appropriate measures to monitor and maintain availability and reliability of the off
    Report CR-2015-009109.
-site and alternate
    The failure to manage the increase in risk associated with the potential for a loss of decay
-ac power systems.
    heat removal during refueling activities is a performance deficiency. The performance
  These activities constitute
    deficiency was more than minor, and therefore a finding, because it was associated with the
d one sample of summer
    procedure quality attribute of the Initiating Events Cornerstone and affected the cornerstone
readiness
    objective to limit the likelihood of events that upset plant stability and challenge critical safety
of off-site and alternate
    functions during shutdown as well as power operations. Using Inspection Manual Chapter
-ac power systems , as defined in Inspection Procedure
    0609, Appendix K, Maintenance Risk Assessment and Risk Management Significance
71111.01.  b. Findings No findings were identified.
    Determination Process, dated May 19, 2005, Flowchart 1, Assessment of Risk Deficit, the
  1 R 04 Equipment Alignment (71111.04)
    inspectors determined the need to calculate the risk deficit to determine the significance of
.1 Partial Walk
    this issue. A senior reactor analyst performed a bounding qualitative assessment and
-Down a. Inspection Scope
    determined the incremental core damage probability deficit was less than 1E-6 and the
The inspectors performed partial system walk
    incremental large early release probability deficit was less than 1E-7, based on the
-downs of the following risk
    availability of additional equipment to mitigate the loss of decay heat removal. In
-significant systems:  August 4, 2016, Unit 2 , turbine driven and motor driven auxiliary feedwater pumps  August 23, 2016, Unit 1, train A 125  
    accordance with Flowchart 1 in Appendix K, because incremental core damage probability
V DC distribution system
    deficit was less than 1E-6 and incremental large early release probability deficit was less
  September 20, 2016, Unit
    than 1E-7, the finding screened as having very low safety significance (Green). The finding
s 1 and 2 , fire protection piping in the service water intake structure
    has a human performance cross-cutting aspect associated with bases for decisions, in that,
 
    the licensee failed to ensure that operations leadership adequately communicate potential
  A-5  The inspectors reviewed the
                                                  A-2
licensee's
 
procedures and system design information to determine the correct lineup for the systems. They visually verified that critical portions of the systems or trains were correctly aligned
  problems with the risk management action to start a safety injection pump when in a mode
for the existing plant configuration
  of applicability for low temperature over pressure protection [H.10]. (Section 4OA2)
These activities constitute d three partial system walk
Cornerstone: Mitigating Systems
-down samples as defined i
* Green. The inspectors identified a non-cited violation of 10 CFR 50.65(a)(2), Requirements
n Inspection Procedure
  for monitoring the effectiveness of maintenance at nuclear power plants. Specifically, the
71111.04. b. Findings No findings were identified
  licensee failed to demonstrate that the performance of the Unit 2 auxiliary feedwater check
.  1 R 05 Fire Protection (71111.05)
  valves was being effectively controlled through the performance of appropriate preventive
.1 Quarterly Inspection
  maintenance. The licensees failure to perform appropriate maintenance resulted in several
a. Inspection Scope
  failures of the check valves. The licensee entered this issue into corrective action program
The inspectors evaluated the licensee's fire
  as CR-2016-008312.
protection program for operational status and material condition. The inspectors focused their inspection
  The licensees failure to effectively monitor the performance of maintenance rule scoped
on four plant areas important to safety
  equipment in accordance with 10 CFR 50.65(a)(2) was a performance deficiency. The
:   August 5, 2016, Fire area 2SC7, Unit 2 turbine driven auxiliary feedwater pump room  September 19, 2016, Fire area SB2a, Unit 1 train A residual heat removal, safety injection, containment spray pumps rooms
  performance deficiency was more than minor, and therefore a finding, because it was
  September 19, 2016, Fire area SE16, Unit 1 Electrical  
  associated with the equipment performance attribute of the Mitigating Systems Cornerstone
Equipment Room  September 19, 2016, Fire area 2SE16, Unit 2 Electrical  
  and affected the cornerstone objective to ensure availability, reliability, and capability of
Equipment Room For each area, the inspectors evaluated the fire plan against defined hazards
  systems that respond to initiating events to prevent undesirable consequences. Specifically,
and defense-in-depth features in the licensee's fire protection program. The inspectors evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions.
  the licensee failed to demonstrate that the performance of the Unit 2 auxiliary feedwater
 
  check valves was being effectively controlled through the performance of appropriate
These activities constitute
  preventive maintenance which resulted in failures of the valves. Using Inspection Manual
d four quarterl y inspection sample
  Chapter (IMC) 0609, Appendix A, The Significance Determination Process (SDP) for
s , as defined in Inspection Procedure 71111.05. b. Findings No findings were identified.
  Findings At-Power, dated June 19, 2012, inspectors determined that this finding was of
 
  very low safety significance (Green) because the finding (1) was not a deficiency affecting
  A-6 .2 Annual Inspection
  the design and qualification of a mitigating structure, system, or component, and did not
  result in a loss of operability or functionality, (2) did not represent a loss of system and/or
  function, (3) did not represent an actual loss of function of at least a single train for longer
  than its allowed outage time, or two separate safety systems out-of-service for longer than
   their technical specification allowed outage time, and (4) did not represent an actual loss of
  function of one or more non-technical specification trains of equipment designated as high
  safety-significant for greater than 24 hours in accordance with the licensees maintenance
  rule program. A cross-cutting aspect was not assigned to this finding because the
  performance deficiency occurred in 1996, and therefore, is not indicative of current licensee
  performance. (Section 1R12)
Licensee-Identified Violations
None
                                                  A-3
 
                                          PLANT STATUS
Unit 1 and Unit 2 began the inspection period at approximately 100 percent power and operated
at that power level for the entire inspection period.
                                        REPORT DETAILS
1.     REACTOR SAFETY
        Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection (71111.01)
.1      Summer Readiness for Offsite and Alternate AC Power Systems
  a.  Inspection Scope
        On July 20, 2016, the inspectors completed an inspection of the stations off-site and
        alternate-ac power systems. The inspectors inspected the material condition of these
        systems, including transformers and other switchyard equipment to verify that plant
        features and procedures were appropriate for operation and continued availability of off-
        site and alternate-ac power systems. The inspectors reviewed outstanding work orders
        and open condition reports for these systems. The inspectors walked down the
        switchyard to observe the material condition of equipment providing off-site power
        sources. The inspectors verified that the licensees procedures included appropriate
        measures to monitor and maintain availability and reliability of the off-site and alternate-
        ac power systems.
        These activities constituted one sample of summer readiness of off-site and alternate-ac
        power systems, as defined in Inspection Procedure 71111.01.
  b.  Findings
        No findings were identified.
1R04 Equipment Alignment (71111.04)
.1     Partial Walk-Down
  a.   Inspection Scope
        The inspectors performed partial system walk-downs of the following risk-significant
        systems:
            *   August 4, 2016, Unit 2, turbine driven and motor driven auxiliary feedwater
                pumps
            *   August 23, 2016, Unit 1, train A 125 VDC distribution system
            *  September 20, 2016, Units 1 and 2, fire protection piping in the service water
                intake structure
                                                A-4
 
      The inspectors reviewed the licensees procedures and system design information to
      determine the correct lineup for the systems. They visually verified that critical portions
      of the systems or trains were correctly aligned for the existing plant configuration.
      These activities constituted three partial system walk-down samples as defined in
      Inspection Procedure 71111.04.
  b. Findings
      No findings were identified.
1R05 Fire Protection (71111.05)
.1   Quarterly Inspection
  a. Inspection Scope
      The inspectors evaluated the licensees fire protection program for operational status
      and material condition. The inspectors focused their inspection on four plant areas
      important to safety:
          *   August 5, 2016, Fire area 2SC7, Unit 2 turbine driven auxiliary feedwater pump
              room
          *   September 19, 2016, Fire area SB2a, Unit 1 train A residual heat removal, safety
              injection, containment spray pumps rooms
          *  September 19, 2016, Fire area SE16, Unit 1 Electrical Equipment Room
          *   September 19, 2016, Fire area 2SE16, Unit 2 Electrical Equipment Room
      For each area, the inspectors evaluated the fire plan against defined hazards and
      defense-in-depth features in the licensees fire protection program. The inspectors
      evaluated control of transient combustibles and ignition sources, fire detection and
      suppression systems, manual firefighting equipment and capability, passive fire
      protection features, and compensatory measures for degraded conditions.
      These activities constituted four quarterly inspection samples, as defined in Inspection
      Procedure 71111.05.
  b. Findings
      No findings were identified.
                                              A-5
 
.2   Annual Inspection
  a. Inspection Scope
      On September 20, 2016, the inspectors completed their annual evaluation of the
      licensees fire brigade performance. This evaluation included observation of two fire
      drills:
          *  March 22, 2016, Unit 1, announced drill, contaminated waste fire drill, 832 foot
              corridor
          *  June 22, 2016, Unit 2, announced drill, 858 foot elevation valve gallery
      During these drills the inspectors evaluated the capability of the fire brigade members,
      the leadership ability of the brigade leader, the brigades use of turnout gear and fire-
      fighting equipment, and the effectiveness of the fire brigades team operation. The
      inspectors also reviewed whether the licensees fire brigade met NRC requirements for
      training, dedicated size and membership, and equipment.
      These activities constituted one annual inspection sample, as defined in Inspection
      Procedure 71111.05.
  b. Findings
      No findings were identified.
1R06 Flood Protection Measures (71111.06)
  a. Inspection Scope
      On September 23, 2016, the inspectors completed an inspection of the stations ability to
      mitigate flooding due to internal causes. After reviewing the licensees flooding analysis,
      the inspectors selected one plant area containing risk-significant structures, systems,
      and components that were susceptible to flooding:
          *  Units 1 and 2, service water intake structure
      The inspectors reviewed plant design features and licensee procedures for coping with
      internal flooding. The inspectors walked down the selected areas to inspect the design
      features, including the material condition of seals, drains, and flood barriers. The
      inspectors evaluated whether operator actions credited for flood mitigation could be
      successfully accomplished.
      These activities constituted completion of one flood protection measures sample as
      defined in Inspection Procedure 71111.06.
  b. Findings
      No findings were identified.
                                              A-6
 
1R11 Licensed Operator Requalification Program and Licensed Operator Performance
      (71111.11)
.1    Review of Licensed Operator Requalification
  a. Inspection Scope
      On September 27, 2016, the inspectors observed a portion of an annual requalification
      test for licensed operators. The inspectors assessed the performance of the operators
      and the evaluators critique of their performance.
      These activities constituted completion of one quarterly licensed operator requalification
      program sample, as defined in Inspection Procedure 71111.11.
  b. Findings
      No findings were identified.
.2    Review of Licensed Operator Performance
  a.  Inspection Scope
      Inspectors observed the performance of on-shift licensed operators in the plants main
      control room. At the time of the observations, the plant was in a period of heightened
      activity or risk due to testing being performed on reactor protection and response to
      unusual plant conditions. The inspectors observed the operators performance of the
      following activities:
          *  July 13, 2016, Unit 2, Observation during slave relay testing
          *  August 8, 2016, Unit 2, Observation of operators response to heater drain pump
              seal water low pressure alarm
          *  September 26, 2016, Unit 1, Observation of reactor trip breaker testing
      In addition, the inspectors assessed the operators adherence to plant procedures,
      including conduct of operations procedure and other operations department policies.
      These activities constituted completion of one quarterly licensed operator performance
      sample, as defined in Inspection Procedure 71111.11.
  b. Findings
      No findings were identified.
1R12 Maintenance Effectiveness (71111.12)
  a. Inspection Scope
      The inspectors reviewed two instances of degraded performance or condition of safety-
      related structures, systems, and components (SSCs):
                                                A-7
 
        *  August 20, 2016, Unit 2, main feedwater system split flow bypass check valves
        *  September 23, 2016, Unit 1, pressurizer heater group C blown fuse
  The inspectors reviewed the extent of condition of possible common cause SSC failures
  and evaluated the adequacy of the licensees corrective actions. The inspectors
  reviewed the licensees work practices to evaluate whether these may have played a
  role in the degradation of the SSCs. The inspectors assessed the licensees
  characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance
  Rule), and verified that the licensee was appropriately tracking degraded performance
  and conditions in accordance with the Maintenance Rule.
  These activities constituted completion of two maintenance effectiveness samples, as
  defined in Inspection Procedure 71111.12.
b. Findings
  Introduction. The inspectors identified a Green, non-cited violation of 10 CFR
  50.65(a)(2), Requirements for monitoring the effectiveness of maintenance at nuclear
  power plants. Specifically, the licensee failed to demonstrate that the performance of
  the Unit 2 auxiliary feedwater check valves was being effectively controlled through the
  performance of appropriate preventive maintenance.
  Description. On November 11, 2015, the licensee conducted in-service testing on
  feedwater check valve 2FW-0191, one of four steam generator split flow bypass check
  valves. During the test, check valve 2FW-0191 failed to meet the sites acceptance
  criteria indicating the valve failed to seat. The licensee stopped the test and initiated
  Condition Report CR-2015-10961 to document the test failure.
  Subsequently, the system engineer performed a maintenance rule functional failure
  review of this issue. This review determined that the failure of valve 2FW-0191 to seat
  was not a maintenance rule functional failure and the function would remain in (a)(2)
  status. Inspectors questioned this assessment because one of the scoped functions of
  this feedwater check valve is to shut to prevent bypassing flow from the steam
  generators. During discussions with the licensee, the inspectors determined that system
  engineer was only evaluating the split flow check valves performance against the main
  feedwater systems criteria to provide feedwater to the steam generator, and not against
  the criteria related to the valves ability to shut to prevent bypassing flow from the steam
  generators. Inspectors also determined that the licensee was not performing
  preventative maintenance on the check valves to ensure their ability to close and seat
  properly.
  The inspectors subsequently reviewed the last test data for all four of the steam
  generator split flow bypass check valves. In this review the inspectors noted that in
  2011 valve 2FW-0192 had failed to meet the established acceptance criteria, yet the
  failure was not noted as a functional failure. Additionally, in 2012, valves 2FW-0191,
  2FW-0192, and 2FW-0193 all failed to meet the established acceptance criteria, and
  again the failures were not noted as functional failures.
  The inspectors noted that 10 CFR 50.65(a)(2) requires, in part, that monitoring as
  specified in 10 CFR 50.65(a)(1) is not required where it has been demonstrated that the
                                              A-8
 
performance of a system is being effectively controlled through the performance of
appropriate preventive maintenance, such that the system remains capable of
performing its intended function. Based on their review, the inspectors determined that
the licensee failed to demonstrate that the performance of the Unit 2 feedwater check
valves was being effectively controlled. Specifically, the licensee was not performing
preventative maintenance on the check valves, resulting in the valves failing to close on
multiple occasions during testing.
The inspectors informed the licensee of the concerns and the licensee initiated condition
report CR-2016-008312 to capture this issue in the stations corrective action program.
The licensee recognized that they were not correctly monitoring the function of these
check valves. Specifically, the licensee determined that monitoring the check valves
only as part of the main feedwater system was not adequate since the systems
performance criteria is to provide feedwater to the steam generators, and the check
valves function is to close to prevent bypass flow. The licensee subsequently performed
a review to determine if other safety-related check valves were also not being monitored
correctly. Based on this review the licensee determined that there were 841 safety-
related check valves (of which 230 were classified as run to failure) that were not being
monitored against their scoped criteria. To correct this issue, the licensee created a new
monitoring function for safety related check valves which monitors the close function,
and moved the equipment to 10 CFR 50.65(a)(1) monitoring requirements because they
determined that they were not able to demonstrate that the performance of the check
valves was being effectively controlled.
Analysis. The licensees failure to effectively monitor the performance of maintenance
rule scoped equipment in accordance with 10 CFR 50.65(a)(2) was a performance
deficiency. The performance deficiency was more than minor, and therefore a finding,
because it was associated with the equipment performance attribute of the Mitigating
Systems Cornerstone and affected the cornerstone objective to ensure availability,
reliability, and capability of systems that respond to initiating events to prevent
undesirable consequences. Specifically, the licensee failed to demonstrate that the
performance of the Unit 2 auxiliary feedwater check valves was being effectively
controlled through the performance of appropriate preventive maintenance which
resulted in failures of the valves. Using Inspection Manual Chapter (IMC) 0609,
Appendix A, The Significance Determination Process (SDP) for Findings At-Power,
dated June 19, 2012, inspectors determined that this finding was of very low safety
significance (Green) because the finding (1) was not a deficiency affecting the design
and qualification of a mitigating structure, system, or component, and did not result in a
loss of operability or functionality, (2) did not represent a loss of system and/or function,
(3) did not represent an actual loss of function of at least a single train for longer than its
allowed outage time, or two separate safety systems out-of-service for longer than their
technical specification allowed outage time, and (4) did not represent an actual loss of
function of one or more non-technical specification trains of equipment designated as
high safety-significant for greater than 24 hours in accordance with the licensees
maintenance rule program. A cross-cutting aspect was not assigned to this finding
because the performance deficiency occurred in 1996 when the steam generator split
flow bypass check valve was initially scoped under the Maintenance Rule, and therefore,
is not indicative of current licensee performance.
Enforcement. Title 10 CFR 50.65(a)(1) requires, in part, that holders of an operating
license shall monitor the performance of systems and components against licensee
                                            A-9
 
    established goals, in a manner sufficient to provide reasonable assurance that such
    structures, systems, and components are capable of fulfilling their intended safety
    functions. 10 CFR 50.65(a)(2) states, in part, that monitoring as specified in 10 CFR
    50.65(a)(1) is not required where it has been demonstrated that the performance of a
    system is being effectively controlled through the performance of appropriate preventive
    maintenance, such that the system remains capable of performing its intended function.
    Contrary to the above, from initial maintenance rule scoping in 1996 to September 2016,
    the licensee did not monitor the performance of the Unit 2 auxiliary feedwater system
    check valves against licensee-established goals in a manner sufficient to provide
    reasonable assurance that the check valves were capable of fulfilling their intended
    safety functions, and the licensee did not demonstrate that the performance of check
    valves was being effectively controlled through the performance of appropriate
    preventive maintenance, such that the system remained capable of performing its
    intended function. In response to this issue the licensee created a new monitoring
    function for safety related check valves, and moved the equipment to 10 CFR
    50.65(a)(1) monitoring requirements pending further review. Since this violation was of
    very low safety significance (Green) and has been entered into the corrective action
    program as Condition Report CR-2016-008312, this violation is being treated as a non-
    cited violation consistent with Section 2.3.2 of the NRC Enforcement Policy.
    (NCV 05000446/2016003-01, Failure to Adequately Monitor Feedwater System Check
    Valve Performance)
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
   a. Inspection Scope
   a. Inspection Scope
On September 20, 2016, the inspectors completed their annual evaluation of the licensee's fire brigade performance. This evaluation included observation of two fire drills:  March 22, 2016, Unit 1
    On July 7, 2016, the inspectors reviewed a risk assessment and the risk management
, announced drill, contaminated waste fire drill, 832 foot corridor  June 22, 2016, Unit 2
    actions taken by the licensee in response to elevated risk associated with performing an
, announced drill, 858 foot elevation valve gallery
    oil sample on spent fuel pool pump X-01.
  During these drills the inspectors evaluated the capability of the fire brigade members, the leadership ability of the brigade leader, the brigade's use of turnout gear and fire
    The inspectors verified that this risk assessment was performed timely and in
-fighting equipment, and the effectiveness of the fire brigade's team operation. The inspectors also reviewed whether the licensee's fire brigade met NRC requirements for training, dedicated size and membership, and equipment.
    accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant
  These activities constitute
    procedures. The inspectors reviewed the accuracy and completeness of the licensees
d one annual inspection sample , as defined in Inspection Procedure 71111.05.  b. Findings No findings were identified.
    risk assessment and verified that the licensee implemented appropriate risk
  1 R 06 Flood Protection Measures (71111.06)
    management actions based on the result of the assessment.
a. Inspection Scope
    The inspectors also observed portions of three emergent work activities that had the
  On September 23, 2016, the inspectors completed an inspection of the station's ability to mitigate flooding due to internal causes.  After reviewing the licensee's flooding analysis, the inspectors selected one plant area containing risk
    potential to affect the functional capability of mitigating systems:
-significant structures, systems, and components that were susceptible to flooding:
          *  August 18, 2016, Unit 2, Steam generator blowdown isolation valve 2-HV-2399
  Unit s 1 and 2, service water intake structure
            elastomer replacement
  The inspectors reviewed plant design features and licensee procedures for coping with
          * September 1, 2016, Units 1 and 2, unanalyzed condition associated with the
internal flooding. The inspectors walked down the selected areas to inspect the design features, including the material condition of seals, drains, and flood barriers. The
            turbine driven auxiliary feedwater pumps
inspectors evaluated whether operator actions credited for flood mitigation could be successfully accomplished.
          *  September 16, 2016, Unit 2, loop A safety chiller emergent maintenance
 
    The inspectors verified that the licensee appropriately developed and followed a work
These activities constitute
    plan for these activities. The inspectors verified that the licensee took precautions to
d completion of  
    minimize the impact of the work activities on unaffected SSCs.
one flood protection measures sample
                                              A-10
as defined in Inspection Procedure
 
71111.06. b. Findings No findings were identified.
    These activities constituted completion of four maintenance risk assessments and
 
    emergent work control inspection samples, as defined in Inspection Procedure 71111.13.
  A-7 1 R 11 Licensed Operator Requalification Program and Licensed Operator Performance (71111.11)
  b. Findings
.1 Review of Licensed Operator Requalification
    No findings were identified.
a. Inspection Scope
1R15 Operability Determinations and Functionality Assessments (71111.15)
On September 27, 2016, the inspectors observed
a portion of an annual requalification test for licensed operators.  The inspectors assessed the performance of the operators
and the evaluators' critique of their performance.
 
These activities constitute
d completion of one quarterly licensed
operator requalification program sample , as defined in Inspection Procedure
71111.11.  b. Findings No findings were identified.
  .2 Review of Licensed Operator Performance
   a. Inspection Scope
   a. Inspection Scope
Inspectors observed the performance of on
    The inspectors reviewed seven operability determinations that the licensee performed
-shift licensed operators in the plant's main control room. At the time of the observations, the plant was in a period of heightened activity or risk due to testing being performed on reactor protection and response
    for degraded or nonconforming SSCs:
  to unusual plant conditions.
        *  March 28, 2016, CR-2016-003089, operability determination for control room air
  The inspectors observed the operators' performance of the following activities:
            conditioner X-01 partial refrigerant charge
  July 13, 2016, Unit 2, Observation during slave relay testing
        * July 12, 2016, CR-2016-006613, operability determination for diesel generator
   
            2-01 86-2 lockout relay actuation
  August 8, 2016, Unit 2, Observation of operators response to heater drain pump  
        * August 22, 2016, CR-2016-007251, operability determination for turbine driven
seal water low pressure alarm
            auxiliary feedwater pump 1-01 indicating light socket/bulb melted
  September 26, 2016, Unit 1, Observation of reactor trip breaker testing
        * August 24, 2016, CR-2016-007653, operability determination for motor driven
 
            auxiliary feedwater pump room heat up analyses
In addition, the inspectors assessed the operators' adherence to plant procedures, including conduct of operations procedure and other operations department policies.
        *  August 31, 2016, CR-2016-007840, operability determination for safety injection
  These activities constitute
            pump 2-01 oil leak
d completion of
        *  September 8, 2016, CR-2016-008000, operability determination for diesel
one quarterly licensed
            generator 2-01 failed KVAR meter
  operator performance sample , a s defined in Inspection Procedure
        * September 21, 2016, CR-2016-007880, operability determination for auxiliary
71111.11.  b. Findings No findings were identified.
            feedwater pumps following identification of an unanalyzed condition
  1 R 12 Maintenance Effectiveness (71111.12)
    The inspectors reviewed the timeliness and technical adequacy of the licensees
a. Inspection Scope The inspectors reviewed  
    evaluations. Where the licensee determined the degraded SSC to be operable the
t wo instances of degraded performance or condition of safety
    inspectors verified that the licensees compensatory measures were appropriate to
-related structures, systems, and components
    provide reasonable assurance of operability. The inspectors verified that the licensee
(SSCs): 
    had considered the effect of other degraded conditions on the operability of the
  A-8  August 20, 2016, Unit 2, main feedwater system split flow bypass check valves
    degraded SSC.
  September 23, 2016, Unit 1, pressurizer heater group C blown fuse
    These activities constituted completion of seven operability and functionality review
  The inspectors reviewed the extent of condition of possible common cause SSC failures and evaluated the adequacy of the licensee's corrective actions. The inspectors reviewed the licensee's work practices to evaluate whether these may have played a role in the degradation of the SSCs. The inspectors assessed the licensee's characterization of the degradation
    samples, as defined in Inspection Procedure 71111.15.
in accordance with 10 CFR 50.65 (the Maintenance Rule), and verified that the licensee was appropriately tracking degraded performance and conditions in accordance with the Maintenance Rule.
  b. Findings
 
    No findings were identified.
These activities constitute
                                              A-11
d completion of  
 
t wo maintenance effectiveness samples , a s defined in Inspection Procedure
1R18 Plant Modifications (71111.18)
71111.12. b. Findings Introduction.  The inspectors identified a Green
.1    Temporary Modifications
, non-cited violation of 10 CFR 50.65(a)(2), "Requirements for monitoring the effectiveness of maintenance at nuclear power plants."
  a. Inspection Scope
  Specifically, the licensee failed to demonstrate that the performance of the Unit 2 auxiliary feedwater check valves was being effectively controlled through the
      On September 15, 2016, the inspectors reviewed a temporary plant modification to
performance of appropriate preventive maintenance.
      remove sentinel valves from the turbine driven auxiliary feedwater pumps on Unit 1
Description. On November 11, 2015, the licensee conducted in
      and 2.
-service testing on feedwater check valve 2FW
      The inspectors verified that the licensee had installed these temporary modifications in
-0191, one of four steam generator split flow bypass check valves.  During the test, check valve 2FW
      accordance with technically adequate design documents. The inspectors verified that
-0191 failed to meet the site's acceptance criteria indicating the valve failed to seat. The licensee stopped the test and initiated Condition Report CR
      these modifications did not adversely impact the operability or availability of affected
-2015-10961 to document the test failure.
      SSCs. The inspectors reviewed design documentation and plant procedures affected by
Subsequently, the system engineer performed a maintenance rule functional failure review of this issue.  This review determined that the failure of valve 2FW
      the modifications to verify the licensee maintained configuration control.
-0191 to seat was not a maintenance rule functional failure and the function would remain in (a)(2)
      These activities constituted completion of one sample of temporary modifications, as
status.  Inspectors questioned this assessment because one of the scoped functions of this feedwater check valve is to shut to prevent bypassing flow from the steam
      defined in Inspection Procedure 71111.18.
generators.  During discussions with the licensee, the inspectors determined that system engineer was only evaluating the split flow check valves performance against the main feedwater system's criteria to provide feedwater to the steam generator, and not against the criteria related to the valve's ability to shut to prevent bypassing flow from the steam generators. Inspectors also determined that the licensee was not performing preventative maintenance on the check valves to ensure their ability to close and seat properly. The inspectors subsequently reviewed the last test data for all four of the steam generator split flow bypass check valves.
  b. Findings
In this review the inspectors noted that in 2011 valve 2FW
      No findings were identified.
-0192 had failed to meet the established acceptance criteria, yet the failure was not noted as a functional failure. Additionally, in 2012 , valves 2FW-0191, 2FW-0192, and 2FW-0193 all failed to meet the established acceptance criteria, and again the failures were not noted as functional failures. 
1R19 Post-Maintenance Testing (71111.19)
The inspectors noted that 10 CFR 50.65(a)(2) requires, in part, that monitoring as specified in 10 CFR 50.65(a)(1) is not required where it has been demonstrated that the 
  a. Inspection Scope
  A-9 performance of a system is being effectively controlled through the performance of appropriate preventive maintenance, such that the system remains capable of performing its intended function.  Based on their review, the inspectors determined that the licensee failed to demonstrate that the performance of the Unit 2 feedwater check
      The inspectors reviewed four post-maintenance testing activities that affected risk-
valves was being effectively controlled.  Specifically, the licensee was not performing preventative maintenance on the check valves, resulting in the valves failing to close on
      significant SSCs:
multiple occasions during testing. 
          *  April 5, 2016, Unit 1, offsite power supply breaker 1EA2-1 post maintenance test
The inspectors informed the licensee of the concerns and the licensee initiated condition report CR-2016-008312 to capture this issue in the station's
          *  May 25, 2016, Unit 1, service water pump 1-01 replacement
corrective action program. The licensee recognized that they were not correctly monitoring the function of these check valves.  Specifically, the
          *  August 23, 2016, Unit 2, Steam generator 2-03 blowdown isolation valve
licensee determined that monitoring the check valves only as part of the main feedwater system was not adequate since the system's performance criteria is to provide feedwater to the steam generators
              2-HV-2399 testing following elastomer replacement
, and the check valves function is to close to prevent bypass flow. The licensee subsequently performed a review to determine if other safety
          *  September 15, 2016, Unit 1 and Unit 2, turbine driven auxiliary feedwater pumps
-related check valves were also not being monitored correctly. Based on this review the licensee determined that there were 841 safety
              following temporary modification
-related check valves (of which 230 were classified as run to failure) that were not being monitored against their scoped criteriaTo correct this issue, the licensee created a new monitoring function for safety related check valves which monitors the close function, and moved the equipment to 10
      The inspectors reviewed licensing and design-basis documents for the SSCs and the
CFR 50.65(a)(1) monitoring requirements because they determined that they were not able to demonstrate that the performance of the check
      maintenance and post-maintenance test procedures. The inspectors observed the
valves was being effectively controlled.
      performance of the post-maintenance tests to verify that the licensee performed the tests
Analysis. The licensee's failure to effectively monitor the performance of maintenance rule scoped equipment in accordance with 10 CFR 50.65(a)(2) was a performance
      in accordance with approved procedures, satisfied the established acceptance criteria,
deficiency.  
      and restored the operability of the affected SSCs.
The performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment performance attribute of the Mitigating
      These activities constituted completion of four post-maintenance testing inspection
Systems Cornerstone and affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.  Specifically, the licensee failed to demonstrate that the
      samples, as defined in Inspection Procedure 71111.19.
performance of the Unit 2 auxiliary feedwater
                                              A-12
check valves was being effectively controlled through the performance of appropriate preventive maintenance which resulted in failures of the valves.  Using Inspection Manual Chapter (IMC) 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At
 
-Power," dated June 19, 2012, inspectors determined that this finding was of very low safety
  b. Findings
significance (Green) because the finding (1) was not a deficiency affecting the design and qualification of a mitigating structure, system, or component, and did not result in a loss of operability or functionality, (2) did not represent a loss of system and/or function, (3) did not represent an actual loss of function of at least a single train for longer than its allowed outage time, or two separate safety systems out
      No findings were identified.
-of-service for longer than their technical specification allowed outage time, and (4) did not represent an actual loss of  
1R22 Surveillance Testing (71111.22)
function of one or more non
  a. Inspection Scope
-technical specification trains of equipment designated as high safety
      The inspectors observed four risk-significant surveillance tests and reviewed test results
-significant for greater than 24 hours in accordance with the licensee's maintenance rule program.
      to verify that these tests adequately demonstrated that the SSCs were capable of
  A cross-cutting aspect was not assigned to this finding because the performance deficiency occurred in 1996
      performing their safety functions:
when the steam generator split flow bypass check valve was initially scoped under the Maintenance Rule, and therefore, is not indicative of current licensee performance.
      Other surveillance tests:
  Enforcement.  Title 10 CFR 50.65(a)(1) requires, in part, that holders of an operating license shall monitor the performance of systems and components against licensee 
          *    May 26, 2016, Unit 1, stroke test of power operated relief valve 1-PCV-456
  A-10 established goals, in a manner sufficient to provide reasonable assurance that such structures, systems, and components are capable of fulfilling their intended safety functions. 10 CFR 50.65(a)(2) states, in part, that monitoring as specified in 10 CFR 50.65(a)(1) is not required where it has been demonstrated that the performance of a
          *    August 5, 2016, Unit 2, start and flow test of the turbine driven auxiliary
system is being effectively controlled through the performance of appropriate preventive maintenance, such that the system remains capable of performing its
              feedwater pump
intended function. Contrary to the above, from initial maintenance rule scoping in 1996 to September 2016, the licensee did not monitor the performance of the Unit 2 auxiliary feedwater system check valves against licensee
          *    August 23, 2016, Unit 1, stroke test of containment sump pump discharge line
-established goals in a manner sufficient to provide reasonable assurance that the check valves were capable of fulfilling their intended
              outside-containment isolation valve 1-HV-5157
safety functions, and the licensee did not demonstrate that the performance of check
          *    September 8, 2016, Unit 2, start test of diesel generator 2-01
valves was being effectively controlled through the performance of appropriate preventive maintenance, such that the system remained capable of performing its
      The inspectors verified that these tests met technical specification requirements, that the
intended function.  In response to this issue the licensee created a new monitoring function for safety related check valves, and moved the equipment to 10 CFR
      licensee performed the tests in accordance with their procedures, and that the results of
50.65(a)(1) monitoring requirements pending further review.  Since this violation was of very low safety significance (Green) and has been entered into the corrective action program as Condition Report CR-2016-008312, this violation
      the test satisfied appropriate acceptance criteria. The inspectors verified that the
is being treated as a non
      licensee restored the operability of the affected SSCs following testing.
-cited violation consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000446/201600 3-0 1, Failure to Adequately Monitor Feedwater System Check Valve Performance
      These activities constituted completion of four surveillance testing inspection samples,
1 R 13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
      as defined in Inspection Procedure 71111.22.
  a. Inspection Scope
  b. Findings
On July 7, 2016, the inspectors reviewed a risk assessment and the risk management actions taken by the licensee in response to elevated risk associated with
      No findings were identified.
performing an oil sample on spent fuel pool pump X
      Cornerstone: Emergency Preparedness
-01. The inspectors verified that this risk assessment was performed timely and in accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant
1EP6 Drill Evaluation (71114.06)
procedures. The inspectors reviewed the accuracy and completeness of the licensee's risk assessment and verified that the licensee implemented appropriate risk management actions based on the result of the assessment.
.1    Emergency Preparedness Drill Observation
 
  aInspection Scope
The inspectors also observed portions of three emergent work activities that had the potential to affect the functional capability of mitigating systems:
      The inspectors observed an emergency preparedness drill on September 28, 2016, to
  August 18, 2016, Unit 2, Steam generator blowdown isolation valve 2
      verify the adequacy and capability of the licensees assessment of drill performance.
-HV-2399 elastomer replacement
      The inspectors reviewed the drill scenario, observed the drill from the simulator and
  September 1, 2016, Unit s 1 and 2, unanalyzed condition associated with the turbine driven auxiliary feedwater pumps
      emergency operations facility, and attended the post-drill critique. The inspectors
  September 16, 2016, Unit 2, loop A safety chiller emergent maintenance
      verified that the licensees emergency classifications, off-site notifications, and protective
 
      action recommendations were appropriate and timely. The inspectors verified that any
The inspectors verified that the licensee appropriately developed and followed a work plan for these activities. The inspectors verified that the licensee took precautions to minimize the impact of the work activities on unaffected SSCs.
                                              A-13
 
 
  A-11 These activities constitute
      emergency preparedness weaknesses were appropriately identified by the licensee in
d completion of four maintenance risk assessments and emergent work control inspection samples , as defined in Inspection Procedure
      the post-drill critique and entered into the corrective action program for resolution.
71111.13.  b. Findings No findings were identified.
      These activities constituted completion of one emergency preparedness drill observation
  1 R 15 Operability Determinations
      sample, as defined in Inspection Procedure 71114.06.
and Functionality Assessments
  b. Findings
(71111.15)
      No findings were identified.
a. Inspection Scope
4.    OTHER ACTIVITIES
The inspectors reviewed seven operability determinations that the licensee performed for degraded or nonconforming SSCs:
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
  March 28, 2016, CR
      Preparedness, Public Radiation Safety, Occupational Radiation Safety, and
-2016-003089, operability determination for control room air conditioner X
      Security
-01 partial refrigerant charge
4OA1 Performance Indicator Verification (71151)
  July 12, 2016, CR
.1    Mitigating Systems Performance Index: Emergency AC Power Systems (MS06)
-2016-006613, operability determination for
  a. Inspection Scope
diesel generator
      The inspectors reviewed the licensees mitigating system performance index data for the
2-01 86-2 lockout relay actuation  August 22, 2016, CR-2016-007251, operability determination
      period of July 1, 2015 through June 30, 2016 to verify the accuracy and completeness of
for turbine driven
      the reported data. The inspectors used definitions and guidance contained in Nuclear
auxiliary feedwater pump 1
      Energy Institute Document 99-02, Regulatory Assessment Performance Indicator
-01 indicating light socket/bulb melted
      Guideline, Revision 7, to determine the accuracy of the reported data.
  August 24, 2016, CR-2016-007653, operability determination for motor driven auxiliary feedwater pump room heat up analyses
      These activities constituted verification of the mitigating system performance index for
  August 31, 2016
      emergency ac power systems for Units 1 and 2, as defined in Inspection
, CR-2016-007840, operability determination for safety injection pump 2-01 oil leak
      Procedure 71151.
  September 8, 2016, CR-2016-008000, operability determination for diesel generator
  b. Findings
2-0 1 failed KVAR meter
      No findings were identified.
  September 21, 2016, CR
.2    Mitigating Systems Performance Index: High Pressure Injection Systems (MS07)
-2016-007880, operability determination for auxiliary feedwater pumps following identification of an unanalyzed condition
  a. Inspection Scope
  The inspectors reviewed the timeliness and technical adequacy of the licensee's evaluations. Where the licensee determined the degraded SSC to be operabl
      The inspectors reviewed the licensees mitigating system performance index data for the
e the inspectors verified that the licensee's compensatory measures were appropriate to provide reasonable assurance of operability.  The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability of the degraded SSC
      period of July 1, 2015 through June 30, 2016 to verify the accuracy and completeness of
.
      the reported data. The inspectors used definitions and guidance contained in Nuclear
These activities constitut
      Energy Institute Document 99-02, Regulatory Assessment Performance Indicator
e d completion of seven operability and functionality review
      Guideline, Revision 7, to determine the accuracy of the reported data.
samples , as defined in Inspection Procedure
      These activities constituted verification of the mitigating system performance index for
71111.15.  b. Findings No findings were identified.
      high pressure injection systems for Units 1 and 2, as defined in Inspection
 
      Procedure 71151.
  A-12 1 R 18 Plant Modifications (71111.18)
                                                A-14
.1 Temporary Modifications
 
a. Inspection Scope
  b.  Findings
On September 15, 2016, the inspectors review
      No findings were identified.
ed a temporary plant modification
.3    Mitigating Systems Performance Index: Heat Removal Systems (MS08)
to remove sentinel valves from the turbine driven auxiliary feedwater pumps on Unit 1
  a.  Inspection Scope
and 2. The inspectors verified that the licensee had installed these temporary modifications in accordance with technically adequate design documents. The inspectors verified that these modifications did not adversely impact the operability or availability of affected SSCs.  The inspectors reviewed design documentation and plant procedures affected by
      The inspectors reviewed the licensees mitigating system performance index data for the
the modifications to verify the licensee maintained configuration control.
      period of July 1, 2015 through June 30, 2016 to verify the accuracy and completeness of
 
      the reported data. The inspectors used definitions and guidance contained in Nuclear
These activities constitute
      Energy Institute Document 99-02, Regulatory Assessment Performance Indicator
d completion of  
      Guideline, Revision 7, to determine the accuracy of the reported data.
one sample of temporary modifications, as defined in Inspection Procedure
      These activities constituted verification of the mitigating system performance index for
71111.18.  b. Findings No findings were identified.
      heat removal systems for Units 1 and 2, as defined in Inspection Procedure 71151.
  1 R 19 Post-Maintenance
  b. Findings
Testing (71111.19)
      No findings were identified.
a. Inspection Sco
4OA2 Problem Identification and Resolution (71152)
pe The inspectors reviewed four post-maintenance testing activities that affected risk
.1    Routine Review
-significant SSCs:
    a. Inspection Scope
  April 5, 2016, Unit 1, offsite power supply breaker 1EA2-1 post maintenance test
      Throughout the inspection period, the inspectors performed daily reviews of items
  May 25, 2016, Unit 1, service water
      entered into the licensees corrective action program and periodically attended the
pump 1-01 replacement
      licensees condition report screening meetings. The inspectors verified that licensee
  August 23, 2016, Unit 2, Steam generator 2
      personnel were identifying problems at an appropriate threshold and entering these
-03 blowdown isolation valve
      problems into the corrective action program for resolution. The inspectors verified that
2-HV-2399 testing following elastomer replacement
      the licensee developed and implemented corrective actions commensurate with the
  September 15, 2016, Unit 1 and Unit 2, turbine driven auxiliary feedwater pumps following temporary modification
      significance of the problems identified. The inspectors also reviewed the licensees
  The inspectors reviewed licensing and design
      problem identification and resolution activities during the performance of the other
-basis documents for the SSCs and
      inspection activities documented in this report.
the maintenance
    b. Findings
and post-maintenance test procedures.
      No findings were identified.
  The inspectors observed the performance of the post
.2    Annual Follow-up of Selected Issues
-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected SSCs
    a. Inspection Scope
. These activities constitute
      The inspectors selected two issues for an in-depth follow-up:
d completion of four post-maintenance
          *  During refueling outage 2RF15, October 2015, and refueling outage 1RF18,
testing inspection samples , a s defined in Inspection Procedure
              May 2016, the licensee credited defense in depth contingency plans, risk
71111.19.  
              assessments with specified risk management actions, for time periods when the
  A-13 b. Findings No findings were identified.
              reactor coolant system would be in a loops not filled condition or when shutdown
  1 R 22 Surveillance Testing (71111.22)
                                                A-15
a. Inspection Scope
 
 
          cooling would be in a reduced availability condition due to the increase in risk for
The inspectors observed four risk-significant surveillance tests and reviewed test results to verify that these tests adequately demonstrated that the SSCs were capable of performing their safety functions:
          the activities.
  Other surveillance tests:
          The inspectors assessed the licensees risk assessments and the specified risk
  May 26, 2016, Unit 1, stroke test of power operated relief valve
          management actions. The inspectors identified that the licensee failed to
1-PCV-456  August 5, 2016, Unit 2, start and flow test of the turbine driven auxiliary feedwater pump
          appropriately manage the risk associated with the activities.
  August 23, 2016, Unit 1, stroke test of
      *  On May 18, 2016, after completion of preventative maintenance on the lube oil
containment sump pump discharge line outside-containme nt isolation valve 1
          cooler for coolant charging pump 1-01, a service water leak was discovered
-HV-5157  September 8, 2016, Unit 2, start test of diesel generator 2
          coming from the cooler head. Upon disassembly, the licensee discovered
-01 
          significant pitting on the head for the heat exchanger. The licensee initiated
The inspectors verified that these test
          Condition Report 2016-004868 to evaluate the issue, though an operability
s met technical specification requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the test satisfied appropriate acceptance criteria. The inspectors verified that the licensee restored the operability of the affected SSCs following testing.
          evaluation was not performed at the time because the unit was not in a mode of
  These activities constitute
          applicability for the charging pump. The licensee determined that this condition
d completion of four surveillance testing inspection samples , as defined in Inspection Procedure
          had been previously identified in Condition Report CR-2014-001804, and parts
71111.22.  b. Findings No findings were identified.
          were on order to replace the pitted head. The licensees corrective action was to
  Cornerstone:  Emergency Preparedness
          apply Loctite #2, a sealant material, to stop the leak, noting that this had
1 EP 6 Drill Evaluation (71114.06)
          previously been evaluated as acceptable in Condition Report CR-2006-001208.
.1 Emergency Preparedness Drill Observation
          Upon further review inspectors determined that the evaluation performed in CR-
a. Inspection Scope
          2006-001208 was a one-time evaluation for use of Loctite #2, and did not
The inspectors observed an emergency preparedness drill on September 28, 2016, to verify the adequacy and capability of the licensee's assessment of drill performance. 
          establish a basis for the current use. Therefore, an operability evaluation was
The inspectors reviewed the drill scenario, observed the drill from the simulator and emergency operations facility, and attended the post
          required for the subsequent use of Loctite. The licensee initiated Condition
-drill critique.  The inspectors verified that the licensee's emergency classifications, off
          Reports CR-2016-004936 and CR-2016-006674 to address this issue, and
-site notifications, and protective action recommendations were appropriate and timely.  The inspectors verified that any 
          documented a current operability evaluation for use of the Loctite.
  A-14 emergency preparedness weaknesses were appropriately identified by the licensee in the post-drill critique and entered into the corrective action program for resolution.
          Inspectors determined that this issue was a minor violation of Title 10 CFR Part
 
          50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, which
These activities constitute
          requires, in part, that activities affecting quality shall be accomplished in
d completion of
          accordance with documented instructions, procedures, or drawings, of a type
one emergency preparedness drill observation sample, as defined in Inspection Procedure
          appropriate to the circumstances. Station Procedure STI-442.01, Operability
71114.06.  b. Findings No findings were identified.
          Determination and Functionality Assessment Program, is an Appendix B quality
  4. OTHER ACTIVITIES
          related procedure that is appropriate to the circumstances for evaluating the
Cornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security 4OA 1 Performance Indicator Verification (71151)
          operability of safety-related components. Station Procedure STI-442.01 step 6.1,
.1 Mitigating Systems Performance Index:
          requires, in part, that when a potential degraded or nonconforming condition is
Emergency AC Power System
          identified, the shift manager should ensure the operability determination process
s (MS06) a. Inspection Scope
          is initiated to determine the operability of the structure, system or component.
The inspectors reviewed the licensee's mitigating system performance index data for the
          The inspectors assessed the licensees problem identification threshold, cause
period of July 1, 2015
          analyses, extent of condition reviews and compensatory actions. The inspectors
through June 30, 2016
          verified that the licensee appropriately prioritized the planned corrective actions
to verify the accuracy and completeness of the reported data.  The inspectors used definitions and guidance contained in
          and that these actions were adequate to correct the condition.
Nuclear Energy Institute Document
  These activities constituted completion of two annual follow-up sample as defined in
99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of the reported
  Inspection Procedure 71152.
data.  These activities constituted verification of the mitigating system performance index for emergency ac power systems for Units 1 and 2, as defined in Inspection Procedure 71151.  b. Findings No findings were identified.
b. Findings
  .2 Mitigating Systems Performance Index: High Pressure Injection Systems (MS07)
  Introduction. The inspectors identified a Green non-cited violation of
a. Inspection Scope
  10 CFR 50.65(a)(4), Requirements for Monitoring the Effectiveness of Maintenance at
The inspectors reviewed the licensee's mitigating system performance index data for the
  Nuclear Power Plants, for the licensees failure to adequately manage the increase in
period of July 1, 2015 through June 30, 2016 to verify the accuracy and completeness of the reported data.  The inspectors used definitions and guidance contained in Nuclear Energy Institute Document
                                            A-16
99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of the reported data.
 
  These activities constituted verification of the mitigating system performance index for high pressure injection systems for Units 1 and 2, as defined in Inspection Procedure 71151. 
risk associated with the potential for a loss of decay heat removal during refueling
  A-15 b. Findings No findings were identified.
outages.
  .3 Mitigating Systems Performance Index
Description. During refueling outage 2RF15, October 2015, when the licensee was
: Heat Removal System
setting up for vacuum fill of the reactor coolant system, inspectors reviewed the stations
s (MS08) a. Inspection Scope
defense in depth contingency plan 2RF15-01. The inspectors determined that this
The inspectors reviewed the licensee's mitigating system performance index data for the period of July 1, 2015 through June 30, 2016 to verify the accuracy and completeness of the reported data.  The inspectors used definitions and
contingency plan was a risk assessment with specified risk management actions for
guidance contained in Nuclear Energy Institute Document
periods when the reactor coolant system would be in a loops not filled condition or
99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of the reported data.
periods of reduced availability of the shutdown cooling system. Inspectors noted that the
 
contingency plan for these periods of increased risk directed that if residual heat removal
These activities constituted verification of the mitigating system performance index for heat removal systems for Units 1 and 2, as defined in Inspection Procedure
(shutdown cooling) is lost, operators should establish alternate cooling flow path using
71151.  b. Findings No findings were identified.
Station Procedure ABN-104, Residual Heat Removal System Malfunction, Revision 9,
  4OA 2 Problem Identification and Resolution
section 8.
(71152) .1 Routine Review
Inspectors reviewed ABN-104, section 8 and noted that it directed operators to start a
a. Inspection Scope
safety injection pump in response to a loss of shutdown cooling. Inspectors identified a
Throughout the inspection period, the inspectors performed daily reviews of
concern that the action to start a safety injection pump would occur while in the mode of
items entered into the licensee's corrective action program
applicability for technical specification 3.4.12, Low Temperature Overpressure
and periodically attended the licensee's condition report screening meetings.  The inspectors verified that licensee personnel were identifying problems at an appropriate threshold and entering these problems into the corrective action program for resolution.  The inspectors verified that the licensee developed and implemented corrective actions commensurate with the significance of the problems identified.
Protection System. Technical specification 3.4.12 requires the safety injection pumps
  The inspectors also reviewed the licensee's problem identification and resolution activities during the performance of the other inspection activities documented in this report.
be made incapable of injecting due to concerns of over pressurizing the reactor coolant
  b. Findings No findings were identified.
system in modes 4, 5, and 6 (the latter only when the reactor vessel head is installed).
  .2 Annual Follow
The licensee initiated Condition Report CR-2015-009109 to capture the inspectors
-up of Selected Issues
concern in the stations corrective action program.
a. Inspection Scope
Subsequently, during refueling outage 1RF18, May 2016, inspectors noted that the
The inspectors selected
licensee again credited a defense in depth contingency plan (1RF18-01) which again
two issue s for an in-depth follow
would have operators start a safety injection pump when technical specification 3.4.12
-up:  During refueling outage 2RF15, October 2015, and refueling outage 1RF18,
was in effect. During subsequent reviews, the inspectors determined that the licensee
May 2016, the licensee credited defense in depth contingency plans, risk assessments with specified risk management actions, for time periods when the reactor coolant system would be in a loops not filled condition or when shutdown 
did not have an evaluation for starting a safety injection pump when low temperature
  A-16 cooling would be in a reduced availability condition due to the increase in risk for the activities
overpressure protection was in effect.
. The inspectors assessed the licensee's risk assessments and the specified risk management actions.  The inspectors identified that the licensee failed to
Inspectors determined that the specified risk management action to start a safety
appropriately manage the risk associated with the activities.
injection pump would restore flow to the core to mitigate the loss of shutdown cooling.
  On May 18, 2016, after completion of preventative maintenance on the lube oil cooler for coolant charging pump 1
However, the inspectors also determined that the plant is not analyzed for using a safety
-01, a service water leak was discovered coming from the cooler head.  Upon disassembly, the licensee discovered
injection pump during periods when the reactor coolant system is at low temperatures
significant pitting on the head
requiring low temperature overpressure protection. The proposed use of safety injection
for the heat exchanger.  The licensee initiated Condition Report 2016
pumps as described in ABN-104, section 8, without analyses for sufficient relief
-004868 to evaluate the issue, though an operability evaluation was not performed at the time because the unit was not in a mode of applicability for the charging pump.  The licensee determined that this condition had been previously identified in Condition Report CR
capability, created the potential for vessel overpressurization and a challenge to the
-2014-001804, and parts were on order to replace the pitted head.  The licensee's corrective action was to apply Loctite #2, a sealant material, to stop the leak, noting that this had previously been evaluated as acceptable in Condition Report CR
reactor coolant system barrier. Any challenge to the reactor coolant system barrier
-2006-001208. 
would serve to increase risk. The inspectors also noted that the licensee had several
Upon further review inspectors determined that the evaluation performed in CR
options to mitigate a potential loss of shutdown cooling that are analyzed during period
-2006-001208 was a one
where low temperature overpressure protection is required. Specifically, the inspectors
-time evaluation for use of Loctite #2, and did not establish a basis for the current use.  Therefore, an operability evaluation was required for the subsequent use of Loctite.  The licensee initiated Condition Reports CR
identified that the licensee could start centrifugal charging pumps to restore core flow
-2016-004936 and CR
following a loss of shutdown cooling. These pumps have slightly less capacity than the
-2016-006674 to address this issue, and document ed a current operability evaluation for use of the Loctite.
safety inspection pumps which would be bounded by the relief capability required in
    Inspectors determined that this issue was a minor violation of Title 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," which requires, in part, that activities affecting quality shall be accomplished in accordance with documented instructions, procedures, or drawings, of a type
appropriate to the circumstances.  Station Procedure STI
-442.01, "Operability Determination and Functionality Assessment Program," is an Appendix B quality related procedure
that is appropriate to the circumstances for evaluating the operability of safety
-related components.  Station Procedure STI
-442.01 step 6.1, requires, in part, that when a potential degraded or nonconforming condition is identified, the shift manager should ensure the operability determination process is initiated to determine the operability of the structure, system or component.
 
The inspectors assessed the licensee's problem identification threshold, cause analyses, extent of condition reviews and compensatory actions.  The inspectors verified that the licensee appropriately prioritized the planned corrective actions
and that these actions were adequate to correct the condition.
 
These activities constitute
d completion of two annual follow
-up sample a s defined i n Inspection Procedure
71152.  b. Findings Introduction.  The inspectors identified a Green non
-cited violation of
10 CFR 50.65(a)(4), "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants," for the licensee's failure to adequately manage the increase in 
  A-17 risk associated with the potential for a loss of decay heat removal during refueling outages.    Description.  During refueling outage 2RF15, October 2015, when the licensee was setting up for vacuum fill of the reactor coolant system
, inspectors reviewed the station
's defense in depth contingency plan 2RF15
-01.  The inspectors determined that this contingency plan was a risk assessment with specified risk management actions for periods when the reactor coolant system would be in a
"loops not filled condition
" or periods of reduced
availability of the shutdown cooling system.  Inspectors noted that the contingency plan for these periods
of increased risk directed that if residual heat removal (shutdown cooling) is lost, operators should establish alternate cooling flow path using Station Procedure ABN
-104, "Residual Heat Removal System Malfunction," Revision 9, section 8.
 
Inspectors reviewed ABN
-104, section 8 and noted that it directed operators to start a safety injection pump
in response to a loss of shutdown cooling.  Inspectors identified
a concern that
the action to start a safety injection pump would occur while in the mode of applicability for technical specification 3.4.12, "Low Temperature Overpressure Protection System
."  Technical specification 3.4.12 requires the safety injection pumps be made incapable of injecting due to concerns of
over pressurizing the reactor coolant system in modes 4, 5, and 6 (the latter only when the reactor vessel head is installed).  The licensee initiated Condition Report CR
-2015-009109 to capture th
e inspector's concern in the station
's corrective action program.  Subsequently, during refueling outage 1RF18, May 2016, inspectors noted that the licensee again credited a defense in depth contingency plan (1RF18
-01) which again would have operators start a safety injection pump when technical specification 3.4.
12 was in effect.  During subsequent reviews, the inspectors determined that the licensee did not have an evaluation for starting a safety injection pump when low temperature overpressure protection was in effect. 
 
Inspectors determined that the specified risk management action to start a safety injection pump would restore flow to the core to mitigate the loss of shutdown cooling.  However, the inspectors also determined that the plant is not analyzed for using a safety injection pump during periods when the reactor coolant system is at low temperatures requiring low temperature overpressure protection.  The proposed use of safety injection
pumps as described in ABN
-104, section 8, without analyses for sufficient relief capability, created the potential for vessel overpressurization and a challenge to the reactor coolant system barrier.  Any challenge to the reactor coolant system barrier
would serve to increase risk.  The inspectors also noted that the licensee had several options to mitigate a potential loss of shutdown cooling that are analyzed during period where low temperature overpressure protection is required.  Specifically, the inspectors
identified that the licensee could start centrifugal charging pumps to restore core flow following a loss of shutdown cooling.  These pumps have slightly less capacity than the safety inspection pumps which would be bounded by the relief capability required in  
technical specification 3.4.12.
technical specification 3.4.12.
 
Inspectors informed the licensee of the additional concerns and the licensee added them
Inspectors informed the licensee of the
to Condition Report CR-2015-009109. Inspectors determined that the licensee had not
additional
started a safety injection pump when technical specification 3.4.12 was in effect during
concerns and the licensee added them to Condition Report CR
                                          A-17
-2015-009109. Inspectors determined that the licensee had not started a safety injection pump when technical specification 3.4.12 was in effect
 
during
1RF19 or 2RF18. As corrective actions, the licensee amended Condition Report
  A-18 1RF19 or 2RF18. As corrective actions, the license
e amend ed Condition Report  
CR-2015-009109 to evaluate appropriate risk management actions.
CR-2015-009109 to evaluate appropriate risk management actions.
  Analyses. The failure to manage the increase in risk associated with the potential for a loss of decay heat removal during refueling activities is a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the procedure quality attribute of the Initiating Events Cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power  
Analyses. The failure to manage the increase in risk associated with the potential for a
operations. Using Inspection Manual Chapter 0609, Appendix K, "Maintenance Risk Assessment and Risk Management Significance Determination Process," dated May 19, 2005, Flowchart 1, "Assessment of Risk Deficit," and determined the need to calculate the risk deficit to determine the significance of this issue. A senior reactor analyst performed a bounding qualitative assessment, using insights from Inspection Manua
loss of decay heat removal during refueling activities is a performance deficiency. The
l Chapter 0609, Appendix G, "Shutdown Operations Significance Determination Process,"
performance deficiency was more than minor, and therefore a finding, because it was
and determined the incremental core damage probability deficit was less than 1E
associated with the procedure quality attribute of the Initiating Events Cornerstone and
-6 and the incremental large early release probability deficit was less than 1E
affected the cornerstone objective to limit the likelihood of events that upset plant
-7. The influential assumptions used by the senior reactor analyst included the low exposure time that the  
stability and challenge critical safety functions during shutdown as well as power
plant is in LTOP conditions, the initiating event frequency associated with a loss of decay heat removal, available operator mitigation
operations. Using Inspection Manual Chapter 0609, Appendix K, Maintenance Risk
actions that would prevent the use of safety injection pumps
Assessment and Risk Management Significance Determination Process, dated May 19,
, and the availability of additional equipment to mitigate the loss of decay heat removal.
2005, Flowchart 1, Assessment of Risk Deficit, and determined the need to calculate
  In accordance with Flowchart 1
the risk deficit to determine the significance of this issue. A senior reactor analyst
in Appendix K, because incremental core damage probability deficit was less than 1E
performed a bounding qualitative assessment, using insights from Inspection Manual
-6 and incremental large early release probability deficit was less than 1E
Chapter 0609, Appendix G, Shutdown Operations Significance Determination Process,
-7, the finding screened as having very low safety significance (Green). The finding has a human performance cross
and determined the incremental core damage probability deficit was less than 1E-6 and
-cutting aspect associated with bases for decisions, in that, the licensee failed
the incremental large early release probability deficit was less than 1E-7. The influential
to ensure that operations leadership adequately communicate potential problems with the risk management action to start a safety injection pump when in a mode of applicability for low temperature over pressure protection [H.10]. Enforcement. Title 10 CFR 50.65(a)(4) requires, in part, that licensees shall asses s and manage the increase in risk that may result from proposed maintenance activities. Defense in depth contingency plan
assumptions used by the senior reactor analyst included the low exposure time that the
s 2RF15-01 and 1RF18
plant is in LTOP conditions, the initiating event frequency associated with a loss of decay
-01 implement pre
heat removal, available operator mitigation actions that would prevent the use of safety
-planned risk assessments and specified risk management actions for times during refueling outages when the reactor coolant system is depressurized and level is lowered. Contrary to the above, from October 3, 2015, through May 31, 2016, the licensee failed to manage the increase in risk from proposed maintenance activities. Specifically, the licensee implemented a risk management action that did not reduce the risk, instead it called for placing the plant in an unanalyzed condition which  
injection pumps, and the availability of additional equipment to mitigate the loss of decay
could elevate risk. As an immediate corrective action the licensee initiated Condition Report CR
heat removal.
-2015-009109 to evaluate appropriate risk management actions. Since this violation was of very low  
In accordance with Flowchart 1 in Appendix K, because incremental core damage
safety significance (Green) and has been entered into the corrective action program as Condition Report  
probability deficit was less than 1E-6 and incremental large early release probability
CR-2015-009109, this violation is being treated as a non
deficit was less than 1E-7, the finding screened as having very low safety significance
-cited violation consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000445/201600
(Green). The finding has a human performance cross-cutting aspect associated with
3-0 2; 05000446/201600
bases for decisions, in that, the licensee failed to ensure that operations leadership
3-0 2, Failure to Manage Risk  
adequately communicate potential problems with the risk management action to start a
During Refueling Outages
safety injection pump when in a mode of applicability for low temperature over pressure
)  
protection [H.10].
  A-19 4OA 5 Other Activities
Enforcement. Title 10 CFR 50.65(a)(4) requires, in part, that licensees shall assess and
a. Inspection Scope The inspectors evaluated the impact of financial conditions on continued safe performance at Comanche Peak. I
manage the increase in risk that may result from proposed maintenance activities.
n that t he licensee's pa r ent c o m pan y , E n e r g y F u t u r e H o l d i n g s , w as under bank
Defense in depth contingency plans 2RF15-01 and 1RF18-01 implement pre-planned
r up t cy p r o t e c t i on/r e o r g an i z a t i on du r i ng t he inspec t i on p e r i o d , NR C R e g io n IV condu c t ed spec ial r e v i e w s of p roce sses a t C o manche P e a k. T he inspec t o r s e v a l ua t ed se v e ral aspec t s o f t he licensee's ope r a ti ons t o d e t e r m i ne w he t her t he f i nanc ial cond i t i on o f t he s t a t i on i m pac t ed p lant s a f e t y. T he f a c t o r s r e v i e w e d i nc luded: (1) i m pa c t on s t a f f i ng, (2) co r r ec t i v e m a i n tenance ba c k l og, (3) chan ges t o t he p l anned m a i n t en ance schedu l e, (4) c o rr e c ti v e ac t i on p r o g r a m i m p l e m en t a t i on, and (5) r educ t i on i n o u t a g e scop e , i nc l ud i ng r i s k-s i g n i f icant m od i f i ca t i on s. I n pa r t i cu l a r , t he inspec t o r s v e r i f i ed t h a t licensee p e rsonnel con
risk assessments and specified risk management actions for times during refueling
t inued t o i den t i f y p r o b l e m s a t an app r o p r i a t e t h resho l d and e n t er these p r ob l e m s i n t o t he c o rr e c ti v e ac t i on p r o g r a m for r e so l u t i on. T he inspec t o r s a lso v e r i f i ed that t he licensee con t i nued t o de v e l op and i m p l e m e n t c o rr e c t i v e ac t ions co mm e n su r a t e w i t h t he s i g n i f icance o f t he p r ob l e m s i de n t i f ied.  T he spec ial r e v i ew of p r ocesses a t C o manche P e ak i nc l uded con t i nuous r e v i e ws by t he R es ident Inspe c t o rs, as w e ll as t he spec i a li st-l ed base li ne inspec t i ons co m p l e t ed du r i n g t he i n s pec t i on pe r i od w h ich a r e doc u m en t ed p r e v i o u s l y i n t h i s r ep o r t. b. Findings No findings were identified.
outages when the reactor coolant system is depressurized and level is lowered.
  4OA 6 Meetings, Including Exit
Contrary to the above, from October 3, 2015, through May 31, 2016, the licensee failed
Exit Meeting Summary
to manage the increase in risk from proposed maintenance activities. Specifically, the
On July 7, 2016, the resident inspectors presented the inspection results to Mr. S. Sewell , Senior Director of Engineering and Regulatory Affairs, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
licensee implemented a risk management action that did not reduce the risk, instead it
 
called for placing the plant in an unanalyzed condition which could elevate risk. As an
 
immediate corrective action the licensee initiated Condition Report CR-2015-009109 to
  A-20 SUPPLEMENTAL INFORMATION
evaluate appropriate risk management actions. Since this violation was of very low
  KEY POINTS OF CONTACT
safety significance (Green) and has been entered into the corrective action program as
  G. Struble, Manager, Operations/Simulator Training  
Condition Report CR-2015-009109, this violation is being treated as a non-cited violation
J. Alldredge, Technician, Radiation Protection
consistent with Section 2.3.2 of the NRC Enforcement Policy.
T. Curtis, Lead Environmental Technician
(NCV 05000445/2016003-02; 05000446/2016003-02, Failure to Manage Risk During
S. Darter, Coordinator, Radiation Protection
Refueling Outages)
S. Dixon, Consulting Licensing Analyst/Regulatory Affairs
                                          A-18
T. Emery, Technician , Radiological Environmental Monitoring Program
 
T. Hope, Manager, Regulatory Affairs
4OA5 Other Activities
B. Knapp, Acting Manager, Radiation Protection
    a. Inspection Scope
M. Macho, Supervi
        The inspectors evaluated the impact of financial conditions on continued safe
sor, Radiation Protection
        performance at Comanche Peak. In that the licensees parent company, Energy Future
S. Peterson, Senior Calibration Laboratory Technician, Radiation Protection
        Holdings, was under bankruptcy protection/reorganization during the inspection period,
K. Powell, Supervisor, Radiation Protection
        NRC Region IV conducted special reviews of processes at Comanche Peak. The
M. Syed, Engineer, Systems Engineer
        inspectors evaluated several aspects of the licensees operations to determine whether
M. Watkins, Lead Technician, Instruments and Controls Maintenance
        the financial condition of the station impacted plant safety. The factors reviewed
J. Barnette, Consultant, Licensing Technologist  
        included: (1) impact on staffing, (2) corrective maintenance backlog, (3) changes to the
S. Bartholomew, Analyst , Emergency Preparedness  
        planned maintenance schedule, (4) corrective action program implementation, and
G. Bryan, Operations Specialist, Emergency Preparedness  
        (5) reduction in outage scope, including risk-significant modifications. In particular, the
K. Faver, Planner , Emergency Preparedness  
        inspectors verified that licensee personnel continued to identify problems at an
R. Fishencord, Planner, Emergency Preparedness  
        appropriate threshold and enter these problems into the corrective action program for
J. Hull, Manager, Emergency Preparedness
        resolution. The inspectors also verified that the licensee continued to develop and
R. Marquez, Planner, Emergency Preparedness  
        implement corrective actions commensurate with the significance of the problems
S. Sewell, Senior Director of Engineering and Regulatory Affairs
        identified.
D. Volkening, Manager, Nuclear Oversight
        The special review of processes at Comanche Peak included continuous reviews by the
T. McCool, Site Vice President
        Resident Inspectors, as well as the specialist-led baseline inspections completed during
B. Knowles, Radiation Protection Staff
        the inspection period which are documented previously in this report.
    LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED  
    b. Findings
  Opened and Closed
        No findings were identified.
05000446/201600 3-0 1 NCV Failure to Adequately Monitor Feedwater System Check Valve Performance
4OA6 Meetings, Including Exit
  (Section 1R12)
Exit Meeting Summary
  05000445/201600
On July 7, 2016, the resident inspectors presented the inspection results to Mr. S. Sewell,
3-0 2;05000446/201600
Senior Director of Engineering and Regulatory Affairs, and other members of the licensee staff.
3-0 2 NCV Failure to Manage Risk  
The licensee acknowledged the issues presented. The licensee confirmed that any proprietary
During Refueling Outages
information reviewed by the inspectors had been returned or destroyed.
  (Section 4OA2)    
                                                A-19
  A-21 LIST OF DOCUMENTS REVIEWED
 
  Section 1R01: Adverse Weather Protection
                              SUPPLEMENTAL INFORMATION
  Procedures
                                  KEY POINTS OF CONTACT
Number Title Revision STA-629 Switchyard Control and Transmission Grid Interface
G. Struble, Manager, Operations/Simulator Training
Section 1R04: Equipment Alignment
J. Alldredge, Technician, Radiation Protection
  Condition Reports CR-2016-007245     Drawings Number Title Revision E1-0020 125V DC One Line Diagram
T. Curtis, Lead Environmental Technician
CP-20 E1-0021 Common Auxiliary Control Fuel and Turbine Buildings Normal 480VC MCCs One Line Diagram
S. Darter, Coordinator, Radiation Protection
CP-22  Procedures
S. Dixon, Consulting Licensing Analyst/Regulatory Affairs
Number Title Revision SOP-904 Fire Protection Main Water Supply and Fire Pumps System
T. Emery, Technician, Radiological Environmental Monitoring Program
16 OPT-215 Class 1E Electrical Systems Operability
T. Hope, Manager, Regulatory Affairs
15  Section 1R05: Fire Protection
B. Knapp, Acting Manager, Radiation Protection
  Condition Reports
M. Macho, Supervisor, Radiation Protection
CR-2016-002654     Drawings Number Title Revision E1-2020 Safeguard Building Fire Detection Plan EL 773'
S. Peterson, Senior Calibration Laboratory Technician, Radiation Protection
-0", 790'-6" and 800'-6" CP-2  Procedures
K. Powell, Supervisor, Radiation Protection
Number Title Revision SAF-104 Inspection of Respiratory Protection Equipment (Maintenance and Repair)
M. Syed, Engineer, Systems Engineer
11 
M. Watkins, Lead Technician, Instruments and Controls Maintenance
  A-22 Procedures
J. Barnette, Consultant, Licensing Technologist
Number Title Revision ABN-901 Fire Protection System Alarms or Malfunctions
S. Bartholomew, Analyst, Emergency Preparedness
2 FPI-103A Fire Preplan Instruction Manual, Unit 1 Safeguards Building Elevation 810'
G. Bryan, Operations Specialist, Emergency Preparedness
-6", Rad. Pen. Area & Elec. Equip. Rm
K. Faver, Planner, Emergency Preparedness
Miscellaneous Documents
R. Fishencord, Planner, Emergency Preparedness
Number Title Revision -- Fire Protection Report
J. Hull, Manager, Emergency Preparedness
30  Work Orders
R. Marquez, Planner, Emergency Preparedness
4789803     Section 1R06: Flood Protection Measures
S. Sewell, Senior Director of Engineering and Regulatory Affairs
  Calculations
D. Volkening, Manager, Nuclear Oversight
Number Title Revision SI-CA-0000-693 Miscellaneous Building  
T. McCool, Site Vice President
- Flooding Analysis
B. Knowles, Radiation Protection Staff
1  Section 1R11: Licensed Operator Requalification Program and Licensed Operator Performance
                    LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
  Procedures
Opened and Closed
Number Title Revision EOP-3.0A Steam Generator Tube Rupture
                                    Failure to Adequately Monitor Feedwater System Check Valve
Section 1R13: Maintenance Risk Assessments and Emergent Work Control
  05000446/2016003-01        NCV
  Condition Reports
                                    Performance (Section 1R12)
CR-2016-007272 CR-2016-000493 CR-2016-007720 CR-2016-007428 CR-2016-007690 Procedures
  05000445/2016003-
Number Title Revision DID XPWR-SFP-01 SFP Cooling During Non
                                    Failure to Manage Risk During Refueling Outages (Section
-Refueling Outage Conditions
  02;05000446/2016003-      NCV
- STI-600.01 Protecting Plant Equipment and Sensitive Equipment Controls
                                    4OA2)
1 MSM-GO-0213 Sway Strut Maintenance
02
1  
                                              A-20
  A-23 Work Orders
 
5320735 5210636     Section 1R15: Operability Determinations and Functionality Assessments
                            LIST OF DOCUMENTS REVIEWED
  Calculations
Section 1R01: Adverse Weather Protection
Number Title Revision 1-EB-302-4 As Built HVAC Calculation  
Procedures
- Auxiliary Feedwater Pump Room Unit 1 Condition Reports
Number           Title                                                         Revision
CR-2016-003089 CR-2016-007251 CR-2016-007653 CR-2016-007840   Work Orders
STA-629           Switchyard Control and Transmission Grid Interface             7
5010266     Section 1R18: Plant Modifications
Section 1R04: Equipment Alignment
  Miscellaneous Documents
Condition Reports
Number Title Revision FDA-2016-000123-01-00 Create Temp Mod FDA to Remove the Sentinel Valves on the Casing of the TDAFW Pump Turbines
CR-2016-007245
00  Work Orders
Drawings
5330786 5330788     Section 1R19: Post
Number           Title                                                         Revision
-Maintenance Testing
E1-0020           125V DC One Line Diagram                                       CP-20
  Condition Reports CR-2016-000493 CR-2016-007559 TR-2016-004759 CR-2016-005744 CR-2016-005216 CR-2016-003163     Drawings Number Title Revision E1-0031-07 6.9 kV Switchgear Bus 1EA2 Breaker 1EA2
E1-0021           Common Auxiliary Control Fuel and Turbine Buildings Normal     CP-22
-2 Schematic Diagram CP-13  
                  480VC MCCs One Line Diagram
  A-24 Procedures
Procedures
Number Title Revision MSM-G0-0213 Sway Strut Maintenance
Number           Title                                                         Revision
1 MSM-G0-4004 Baker On-line Motor Testing
SOP-904           Fire Protection Main Water Supply and Fire Pumps System       16
5 MSM-C0-7310 Service Water Pump Maintenance
OPT-215           Class 1E Electrical Systems Operability                       15
5 SOP-603A 6900 V Switchgear
Section 1R05: Fire Protection
16 MSE-G0-0020 Relay Calibration
Condition Reports
Work Orders
CR-2016-002654
5210636 5330786 4297555 5008028 4947477 4986918 5008083 5136434 4913385   Section 1R22: Surveillance Testing
Drawings
  Condition Reports
Number           Title                                                         Revision
CR-2016-007588     Drawings Number Title Revision M2-0206 Flow Diagram Auxiliary Feedwater System
E1-2020           Safeguard Building Fire Detection Plan EL 773-0, 790-6 and CP-2
CP-15 Procedures
                  800-6
Number Title Revision OPT-206B AFW System
Procedures
22 OPT-503A Cntmt Isol Valves ASME Testing
Number           Title                                                         Revision
15  Work Orders
SAF-104           Inspection of Respiratory Protection Equipment (Maintenance   11
5270846    
                  and Repair)
Section 1EP6: Drill Evaluation
                                            A-21
  Procedures
 
Number Title Revision EPP-121 Re-Entry, Recovery and Closeout
Procedures
10 EPP-116 Emergency Repair & Damage Control and Immediate Entries
Number           Title                                                       Revision
  9
ABN-901           Fire Protection System Alarms or Malfunctions               2
  A-25 Procedures
FPI-103A         Fire Preplan Instruction Manual, Unit 1 Safeguards Building 4
Number Title Revision EPP-109 Duties and Responsibilities of the Emergency Coordinator / Recovery Manager
                  Elevation 810-6, Rad. Pen. Area & Elec. Equip. Rm
15 ABN-907 Acts of Nature
Miscellaneous Documents
15  Section 4OA2: Problem Identification and Resolution
Number           Title                                                       Revision
  Condition Reports
--               Fire Protection Report                                     30
CR-2006-001208 CR-2014-001804 CR-2016-004868 CR-2016-004936
Work Orders
4789803
Section 1R06: Flood Protection Measures
Calculations
Number           Title                                                       Revision
SI-CA-0000-693   Miscellaneous Building - Flooding Analysis                 1
Section 1R11: Licensed Operator Requalification Program and Licensed Operator
Performance
Procedures
Number           Title                                                       Revision
EOP-3.0A         Steam Generator Tube Rupture                               9
Section 1R13: Maintenance Risk Assessments and Emergent Work Control
Condition Reports
CR-2016-007272 CR-2016-000493 CR-2016-007720 CR-2016-007428 CR-2016-007690
Procedures
Number           Title                                                       Revision
DID XPWR-SFP- SFP Cooling During Non-Refueling Outage Conditions             -
01
STI-600.01       Protecting Plant Equipment and Sensitive Equipment Controls 1
MSM-GO-0213       Sway Strut Maintenance                                     1
                                            A-22
 
Work Orders
5320735           5210636
Section 1R15: Operability Determinations and Functionality Assessments
Calculations
Number           Title                                                     Revision
1-EB-302-4       As Built HVAC Calculation - Auxiliary Feedwater Pump Room 5
                  Unit 1
Condition Reports
CR-2016-003089 CR-2016-007251 CR-2016-007653 CR-2016-007840
Work Orders
5010266
Section 1R18: Plant Modifications
Miscellaneous Documents
Number           Title                                                     Revision
FDA-2016-         Create Temp Mod FDA to Remove the Sentinel Valves on the 00
000123-01-00      Casing of the TDAFW Pump Turbines
Work Orders
5330786           5330788
Section 1R19: Post-Maintenance Testing
Condition Reports
CR-2016-000493 CR-2016-007559 TR-2016-004759 CR-2016-005744 CR-2016-005216
CR-2016-003163
Drawings
Number           Title                                                     Revision
E1-0031-07       6.9 kV Switchgear Bus 1EA2 Breaker 1EA2-2 Schematic       CP-13
                  Diagram
                                          A-23
 
Procedures
Number           Title                                                   Revision
MSM-G0-0213       Sway Strut Maintenance                                   1
MSM-G0-4004       Baker On-line Motor Testing                             5
MSM-C0-7310       Service Water Pump Maintenance                           5
SOP-603A         6900 V Switchgear                                       16
MSE-G0-0020       Relay Calibration                                       5
Work Orders
5210636           5330786           4297555         5008028       4947477
4986918           5008083           5136434         4913385
Section 1R22: Surveillance Testing
Condition Reports
CR-2016-007588
Drawings
Number           Title                                                   Revision
M2-0206           Flow Diagram Auxiliary Feedwater System                 CP-15
Procedures
Number           Title                                                   Revision
OPT-206B         AFW System                                               22
OPT-503A         Cntmt Isol Valves ASME Testing                           15
Work Orders
5270846
Section 1EP6: Drill Evaluation
Procedures
Number           Title                                                   Revision
EPP-121           Re-Entry, Recovery and Closeout                         10
EPP-116           Emergency Repair & Damage Control and Immediate Entries  9
                                          A-24
 
Procedures
Number           Title                                                     Revision
EPP-109           Duties and Responsibilities of the Emergency Coordinator / 15
                  Recovery Manager
ABN-907           Acts of Nature                                             15
Section 4OA2: Problem Identification and Resolution
Condition Reports
CR-2006-001208 CR-2014-001804 CR-2016-004868 CR-2016-004936
                                            A-25
}}
}}

Latest revision as of 12:13, 30 October 2019

NRC Integrated Inspection Report 05000445/2016003 and 05000446/2016003
ML16314C026
Person / Time
Site: Comanche Peak  Luminant icon.png
Issue date: 11/08/2016
From: Jeremy Groom
NRC/RGN-IV/DRP/RPB-A
To: Peters K
TEX Operations Company
JEREMY GROOM
References
IR 2016003
Download: ML16314C026 (29)


See also: IR 05000445/2016003

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION IV

1600 E. LAMAR BLVD.

ARLINGTON, TX 76011-4511

November 8, 2016

Mr. Ken Peters, Senior Vice President

and Chief Nuclear Officer

TEX Operations Company LLC

P.O. Box 1002

Glen Rose, TX 76043

SUBJECT: COMANCHE PEAK NUCLEAR POWER PLANT - NRC INTEGRATED

INSPECTION REPORT 05000445/2016003 and 05000446/2016003

Dear Mr. Peters:

On September 30, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Comanche Peak Nuclear Power Plant, Units 1 and 2. On September 29,

2016, the NRC inspectors discussed the results of this inspection with Mr. S. Sewell, Senior

Director of Engineering and Regulatory Affairs, and other members of your staff. Inspectors

documented the results of this inspection in the enclosed inspection report.

NRC inspectors documented two findings of very low safety significance (Green) in this report.

All of these findings involved violations of NRC requirements.

If you contest the violations or significance of these NCVs, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with

copies to the Regional Administrator, Region IV; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC resident

inspector at the Comanche Peak Nuclear Power Plant, Units 1 and 2.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region IV; and the NRC resident inspector at the

Comanche Peak Nuclear Power Plant, Units 1 and 2.

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public

Inspections, Exemptions, Requests for Withholding, a copy of this letter, its enclosure, and your

response (if any) will be available electronically for public inspection in the NRCs Public

Document Room or from the Publicly Available Records (PARS) component of the NRC's

K. Peters -2-

Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible

from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic

Reading Room).

Sincerely,

/RA/

Jeremy R. Groom, Branch Chief

Project Branch A

Division of Reactor Projects

Docket Nos. 50-445 and 50-446

License Nos. NPF-87 and NPF-89

Enclosure:

Inspection Report 05000445/2016003 and

05000446/2016003

w/ Attachment: Supplemental Information

cc w/ encl: Electronic Distribution

SUNSI Review ADAMS Non-Sensitive Publicly Available Keyword:

By: JRG Yes No Sensitive Non-Publicly Available NRC-002

OFFICE SRI:DRP/A RI:DRP/A SPE:DRP/A BC:EB1 BC:EB2 BC:OB BC:PSB2

NAME JJosey RKumana RAlexander TFarnholtz GWerner VGaddy HGepford

SIGNATURE /RA/ /RA/ /RA/ /RA/ /RA/ /RA/ /RA/

DATE 10/21/16 10/24/16 10/19/16 10/19/16 10/25/16 10/20/16 10/20/16

OFFICE TL-IPAT BC:DRP/A

NAME THipschman JGroom

SIGNATURE /RA/ /RA/

DATE 10/19/16 11/8/16

Letter to Ken Peters from Jeremy Groom dated November 8, 2016

SUBJECT: COMANCHE PEAK NUCLEAR POWER PLANT-NRC INTEGRATED

INSPECTION REPORT 05000445/2016003 and 05000446/2016003

DISTRIBUTION:

Regional Administrator (Kriss.Kennedy@nrc.gov)

Deputy Regional Administrator (Scott.Morris@nrc.gov)

DRP Director (Troy.Pruett@nrc.gov)

DRP Deputy Director (Ryan.Lantz@nrc.gov)

DRS Director (Anton.Vegel@nrc.gov)

DRS Deputy Director (Jeff.Clark@nrc.gov)

Senior Resident Inspector (Jeffrey.Josey@nrc.gov)

Resident Inspector (Rayomand.Kumana@nrc.gov)

Administrative Assistant (VACANT)

Branch Chief, DRP/A (Jeremy.Groom@nrc.gov)

Senior Project Engineer, DRP/A (Ryan.Alexander@nrc.gov)

Project Engineer, DRP/A (Thomas.Sullivan@nrc.gov)

Project Engineer, DRP/A (Mathew.Kirk@nrc.gov)

Public Affairs Officer (Victor.Dricks@nrc.gov)

Project Manager (Margaret.Watford@nrc.gov)

Team Leader, DRS/IPAT (Thomas.Hipschman@nrc.gov)

RITS Coordinator (Marisa.Herrera@nrc.gov)

ACES (R4Enforcement.Resource@nrc.gov)

Regional Counsel (Karla.Fuller@nrc.gov)

Congressional Affairs Officer (Jenny.Weil@nrc.gov)

RIV Congressional Affairs Officer (Angel.Moreno@nrc.gov)

RIV/ETA: OEDO (Jeremy.Bowen@nrc.gov)

ROPreports

Electronic Distribution for Comanche Peak Nuclear Power Plant

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 05000445, 05000446

License: NPF-87, NPF-89

Report: 05000445/2016003 and 05000446/2016003

Licensee: TEX Operations Company, LLC

Facility: Comanche Peak Nuclear Power Plant, Units 1 and 2

Location: 6322 N. FM-56, Glen Rose, Texas

Dates: July 1 through September 30, 2016

Inspectors: J. Josey, Senior Resident Inspector

R. Kumana, Resident Inspector

W. Cullum, Reactor Inspector

Approved Jeremy R. Groom

By: Chief, Project Branch A

Division of Reactor Projects

A-1 Attachment

SUMMARY

IR 05000445/2016003 and 05000446/2016003; 07/01/2016 - 09/30/2016; Comanche Peak

NPP, Units 1 and 2; Maintenance Effectiveness, Problem Identification and Resolution

The inspection activities described in this report were performed between July 1, 2016, through

September 30, 2016, by the resident inspectors at the Comanche Peak Nuclear Power Plant

and an inspector from the NRCs Region IV office. Two findings of very low safety significance

(Green) are documented in this report. Both of these findings involved a violation of NRC

requirements. The significance of inspection findings is indicated by their color (Green, White,

Yellow, or Red), which is determined using Inspection Manual Chapter 0609, Significance

Determination Process. Their cross-cutting aspects are determined using Inspection Manual

Chapter 0310, Aspects within the Cross-Cutting Areas. Violations of NRC requirements are

dispositioned in accordance with the NRC Enforcement Policy. The NRCs program for

overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process.

Cornerstone: Initiating Events

  • Green. The inspectors identified a non-cited violation of 10 CFR 50.65(a)(4), Requirements

for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, for the licensees

failure to adequately manage the increase in risk associated with the potential for a loss of

decay heat removal during refueling outages. Specifically, the licensee implemented a risk

management action that did not reduce the risk, but instead called for placing a safety

injection pump in service during periods where this action is prohibited by plants technical

specifications for low temperature over pressure protection. The inspectors determined this

was an ineffective risk management action because the use of a safety injection pump

during low pressure and temperature conditions would place the plant in an unanalyzed

condition, resulting in an increase in risk. As an immediate corrective action, the licensee

initiated Condition Report CR-2015-009109 to evaluate appropriate risk management

actions. This finding was entered into the licensees corrective action program as Condition

Report CR-2015-009109.

The failure to manage the increase in risk associated with the potential for a loss of decay

heat removal during refueling activities is a performance deficiency. The performance

deficiency was more than minor, and therefore a finding, because it was associated with the

procedure quality attribute of the Initiating Events Cornerstone and affected the cornerstone

objective to limit the likelihood of events that upset plant stability and challenge critical safety

functions during shutdown as well as power operations. Using Inspection Manual Chapter 0609, Appendix K, Maintenance Risk Assessment and Risk Management Significance

Determination Process, dated May 19, 2005, Flowchart 1, Assessment of Risk Deficit, the

inspectors determined the need to calculate the risk deficit to determine the significance of

this issue. A senior reactor analyst performed a bounding qualitative assessment and

determined the incremental core damage probability deficit was less than 1E-6 and the

incremental large early release probability deficit was less than 1E-7, based on the

availability of additional equipment to mitigate the loss of decay heat removal. In

accordance with Flowchart 1 in Appendix K, because incremental core damage probability

deficit was less than 1E-6 and incremental large early release probability deficit was less

than 1E-7, the finding screened as having very low safety significance (Green). The finding

has a human performance cross-cutting aspect associated with bases for decisions, in that,

the licensee failed to ensure that operations leadership adequately communicate potential

A-2

problems with the risk management action to start a safety injection pump when in a mode

of applicability for low temperature over pressure protection [H.10]. (Section 4OA2)

Cornerstone: Mitigating Systems

  • Green. The inspectors identified a non-cited violation of 10 CFR 50.65(a)(2), Requirements

for monitoring the effectiveness of maintenance at nuclear power plants. Specifically, the

licensee failed to demonstrate that the performance of the Unit 2 auxiliary feedwater check

valves was being effectively controlled through the performance of appropriate preventive

maintenance. The licensees failure to perform appropriate maintenance resulted in several

failures of the check valves. The licensee entered this issue into corrective action program

as CR-2016-008312.

The licensees failure to effectively monitor the performance of maintenance rule scoped

equipment in accordance with 10 CFR 50.65(a)(2) was a performance deficiency. The

performance deficiency was more than minor, and therefore a finding, because it was

associated with the equipment performance attribute of the Mitigating Systems Cornerstone

and affected the cornerstone objective to ensure availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences. Specifically,

the licensee failed to demonstrate that the performance of the Unit 2 auxiliary feedwater

check valves was being effectively controlled through the performance of appropriate

preventive maintenance which resulted in failures of the valves. Using Inspection Manual

Chapter (IMC) 0609, Appendix A, The Significance Determination Process (SDP) for

Findings At-Power, dated June 19, 2012, inspectors determined that this finding was of

very low safety significance (Green) because the finding (1) was not a deficiency affecting

the design and qualification of a mitigating structure, system, or component, and did not

result in a loss of operability or functionality, (2) did not represent a loss of system and/or

function, (3) did not represent an actual loss of function of at least a single train for longer

than its allowed outage time, or two separate safety systems out-of-service for longer than

their technical specification allowed outage time, and (4) did not represent an actual loss of

function of one or more non-technical specification trains of equipment designated as high

safety-significant for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in accordance with the licensees maintenance

rule program. A cross-cutting aspect was not assigned to this finding because the

performance deficiency occurred in 1996, and therefore, is not indicative of current licensee

performance. (Section 1R12)

Licensee-Identified Violations

None

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PLANT STATUS

Unit 1 and Unit 2 began the inspection period at approximately 100 percent power and operated

at that power level for the entire inspection period.

REPORT DETAILS

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

.1 Summer Readiness for Offsite and Alternate AC Power Systems

a. Inspection Scope

On July 20, 2016, the inspectors completed an inspection of the stations off-site and

alternate-ac power systems. The inspectors inspected the material condition of these

systems, including transformers and other switchyard equipment to verify that plant

features and procedures were appropriate for operation and continued availability of off-

site and alternate-ac power systems. The inspectors reviewed outstanding work orders

and open condition reports for these systems. The inspectors walked down the

switchyard to observe the material condition of equipment providing off-site power

sources. The inspectors verified that the licensees procedures included appropriate

measures to monitor and maintain availability and reliability of the off-site and alternate-

ac power systems.

These activities constituted one sample of summer readiness of off-site and alternate-ac

power systems, as defined in Inspection Procedure 71111.01.

b. Findings

No findings were identified.

1R04 Equipment Alignment (71111.04)

.1 Partial Walk-Down

a. Inspection Scope

The inspectors performed partial system walk-downs of the following risk-significant

systems:

pumps

  • August 23, 2016, Unit 1, train A 125 VDC distribution system
  • September 20, 2016, Units 1 and 2, fire protection piping in the service water

intake structure

A-4

The inspectors reviewed the licensees procedures and system design information to

determine the correct lineup for the systems. They visually verified that critical portions

of the systems or trains were correctly aligned for the existing plant configuration.

These activities constituted three partial system walk-down samples as defined in

Inspection Procedure 71111.04.

b. Findings

No findings were identified.

1R05 Fire Protection (71111.05)

.1 Quarterly Inspection

a. Inspection Scope

The inspectors evaluated the licensees fire protection program for operational status

and material condition. The inspectors focused their inspection on four plant areas

important to safety:

room

injection, containment spray pumps rooms

  • September 19, 2016, Fire area SE16, Unit 1 Electrical Equipment Room
  • September 19, 2016, Fire area 2SE16, Unit 2 Electrical Equipment Room

For each area, the inspectors evaluated the fire plan against defined hazards and

defense-in-depth features in the licensees fire protection program. The inspectors

evaluated control of transient combustibles and ignition sources, fire detection and

suppression systems, manual firefighting equipment and capability, passive fire

protection features, and compensatory measures for degraded conditions.

These activities constituted four quarterly inspection samples, as defined in Inspection

Procedure 71111.05.

b. Findings

No findings were identified.

A-5

.2 Annual Inspection

a. Inspection Scope

On September 20, 2016, the inspectors completed their annual evaluation of the

licensees fire brigade performance. This evaluation included observation of two fire

drills:

  • March 22, 2016, Unit 1, announced drill, contaminated waste fire drill, 832 foot

corridor

  • June 22, 2016, Unit 2, announced drill, 858 foot elevation valve gallery

During these drills the inspectors evaluated the capability of the fire brigade members,

the leadership ability of the brigade leader, the brigades use of turnout gear and fire-

fighting equipment, and the effectiveness of the fire brigades team operation. The

inspectors also reviewed whether the licensees fire brigade met NRC requirements for

training, dedicated size and membership, and equipment.

These activities constituted one annual inspection sample, as defined in Inspection

Procedure 71111.05.

b. Findings

No findings were identified.

1R06 Flood Protection Measures (71111.06)

a. Inspection Scope

On September 23, 2016, the inspectors completed an inspection of the stations ability to

mitigate flooding due to internal causes. After reviewing the licensees flooding analysis,

the inspectors selected one plant area containing risk-significant structures, systems,

and components that were susceptible to flooding:

The inspectors reviewed plant design features and licensee procedures for coping with

internal flooding. The inspectors walked down the selected areas to inspect the design

features, including the material condition of seals, drains, and flood barriers. The

inspectors evaluated whether operator actions credited for flood mitigation could be

successfully accomplished.

These activities constituted completion of one flood protection measures sample as

defined in Inspection Procedure 71111.06.

b. Findings

No findings were identified.

A-6

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

(71111.11)

.1 Review of Licensed Operator Requalification

a. Inspection Scope

On September 27, 2016, the inspectors observed a portion of an annual requalification

test for licensed operators. The inspectors assessed the performance of the operators

and the evaluators critique of their performance.

These activities constituted completion of one quarterly licensed operator requalification

program sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

.2 Review of Licensed Operator Performance

a. Inspection Scope

Inspectors observed the performance of on-shift licensed operators in the plants main

control room. At the time of the observations, the plant was in a period of heightened

activity or risk due to testing being performed on reactor protection and response to

unusual plant conditions. The inspectors observed the operators performance of the

following activities:

  • July 13, 2016, Unit 2, Observation during slave relay testing
  • August 8, 2016, Unit 2, Observation of operators response to heater drain pump

seal water low pressure alarm

  • September 26, 2016, Unit 1, Observation of reactor trip breaker testing

In addition, the inspectors assessed the operators adherence to plant procedures,

including conduct of operations procedure and other operations department policies.

These activities constituted completion of one quarterly licensed operator performance

sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors reviewed two instances of degraded performance or condition of safety-

related structures, systems, and components (SSCs):

A-7

  • September 23, 2016, Unit 1, pressurizer heater group C blown fuse

The inspectors reviewed the extent of condition of possible common cause SSC failures

and evaluated the adequacy of the licensees corrective actions. The inspectors

reviewed the licensees work practices to evaluate whether these may have played a

role in the degradation of the SSCs. The inspectors assessed the licensees

characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance

Rule), and verified that the licensee was appropriately tracking degraded performance

and conditions in accordance with the Maintenance Rule.

These activities constituted completion of two maintenance effectiveness samples, as

defined in Inspection Procedure 71111.12.

b. Findings

Introduction. The inspectors identified a Green, non-cited violation of 10 CFR

50.65(a)(2), Requirements for monitoring the effectiveness of maintenance at nuclear

power plants. Specifically, the licensee failed to demonstrate that the performance of

the Unit 2 auxiliary feedwater check valves was being effectively controlled through the

performance of appropriate preventive maintenance.

Description. On November 11, 2015, the licensee conducted in-service testing on

feedwater check valve 2FW-0191, one of four steam generator split flow bypass check

valves. During the test, check valve 2FW-0191 failed to meet the sites acceptance

criteria indicating the valve failed to seat. The licensee stopped the test and initiated

Condition Report CR-2015-10961 to document the test failure.

Subsequently, the system engineer performed a maintenance rule functional failure

review of this issue. This review determined that the failure of valve 2FW-0191 to seat

was not a maintenance rule functional failure and the function would remain in (a)(2)

status. Inspectors questioned this assessment because one of the scoped functions of

this feedwater check valve is to shut to prevent bypassing flow from the steam

generators. During discussions with the licensee, the inspectors determined that system

engineer was only evaluating the split flow check valves performance against the main

feedwater systems criteria to provide feedwater to the steam generator, and not against

the criteria related to the valves ability to shut to prevent bypassing flow from the steam

generators. Inspectors also determined that the licensee was not performing

preventative maintenance on the check valves to ensure their ability to close and seat

properly.

The inspectors subsequently reviewed the last test data for all four of the steam

generator split flow bypass check valves. In this review the inspectors noted that in

2011 valve 2FW-0192 had failed to meet the established acceptance criteria, yet the

failure was not noted as a functional failure. Additionally, in 2012, valves 2FW-0191,

2FW-0192, and 2FW-0193 all failed to meet the established acceptance criteria, and

again the failures were not noted as functional failures.

The inspectors noted that 10 CFR 50.65(a)(2) requires, in part, that monitoring as

specified in 10 CFR 50.65(a)(1) is not required where it has been demonstrated that the

A-8

performance of a system is being effectively controlled through the performance of

appropriate preventive maintenance, such that the system remains capable of

performing its intended function. Based on their review, the inspectors determined that

the licensee failed to demonstrate that the performance of the Unit 2 feedwater check

valves was being effectively controlled. Specifically, the licensee was not performing

preventative maintenance on the check valves, resulting in the valves failing to close on

multiple occasions during testing.

The inspectors informed the licensee of the concerns and the licensee initiated condition

report CR-2016-008312 to capture this issue in the stations corrective action program.

The licensee recognized that they were not correctly monitoring the function of these

check valves. Specifically, the licensee determined that monitoring the check valves

only as part of the main feedwater system was not adequate since the systems

performance criteria is to provide feedwater to the steam generators, and the check

valves function is to close to prevent bypass flow. The licensee subsequently performed

a review to determine if other safety-related check valves were also not being monitored

correctly. Based on this review the licensee determined that there were 841 safety-

related check valves (of which 230 were classified as run to failure) that were not being

monitored against their scoped criteria. To correct this issue, the licensee created a new

monitoring function for safety related check valves which monitors the close function,

and moved the equipment to 10 CFR 50.65(a)(1) monitoring requirements because they

determined that they were not able to demonstrate that the performance of the check

valves was being effectively controlled.

Analysis. The licensees failure to effectively monitor the performance of maintenance

rule scoped equipment in accordance with 10 CFR 50.65(a)(2) was a performance

deficiency. The performance deficiency was more than minor, and therefore a finding,

because it was associated with the equipment performance attribute of the Mitigating

Systems Cornerstone and affected the cornerstone objective to ensure availability,

reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. Specifically, the licensee failed to demonstrate that the

performance of the Unit 2 auxiliary feedwater check valves was being effectively

controlled through the performance of appropriate preventive maintenance which

resulted in failures of the valves. Using Inspection Manual Chapter (IMC) 0609,

Appendix A, The Significance Determination Process (SDP) for Findings At-Power,

dated June 19, 2012, inspectors determined that this finding was of very low safety

significance (Green) because the finding (1) was not a deficiency affecting the design

and qualification of a mitigating structure, system, or component, and did not result in a

loss of operability or functionality, (2) did not represent a loss of system and/or function,

(3) did not represent an actual loss of function of at least a single train for longer than its

allowed outage time, or two separate safety systems out-of-service for longer than their

technical specification allowed outage time, and (4) did not represent an actual loss of

function of one or more non-technical specification trains of equipment designated as

high safety-significant for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in accordance with the licensees

maintenance rule program. A cross-cutting aspect was not assigned to this finding

because the performance deficiency occurred in 1996 when the steam generator split

flow bypass check valve was initially scoped under the Maintenance Rule, and therefore,

is not indicative of current licensee performance.

Enforcement. Title 10 CFR 50.65(a)(1) requires, in part, that holders of an operating

license shall monitor the performance of systems and components against licensee

A-9

established goals, in a manner sufficient to provide reasonable assurance that such

structures, systems, and components are capable of fulfilling their intended safety

functions. 10 CFR 50.65(a)(2) states, in part, that monitoring as specified in 10 CFR

50.65(a)(1) is not required where it has been demonstrated that the performance of a

system is being effectively controlled through the performance of appropriate preventive

maintenance, such that the system remains capable of performing its intended function.

Contrary to the above, from initial maintenance rule scoping in 1996 to September 2016,

the licensee did not monitor the performance of the Unit 2 auxiliary feedwater system

check valves against licensee-established goals in a manner sufficient to provide

reasonable assurance that the check valves were capable of fulfilling their intended

safety functions, and the licensee did not demonstrate that the performance of check

valves was being effectively controlled through the performance of appropriate

preventive maintenance, such that the system remained capable of performing its

intended function. In response to this issue the licensee created a new monitoring

function for safety related check valves, and moved the equipment to 10 CFR

50.65(a)(1) monitoring requirements pending further review. Since this violation was of

very low safety significance (Green) and has been entered into the corrective action

program as Condition Report CR-2016-008312, this violation is being treated as a non-

cited violation consistent with Section 2.3.2 of the NRC Enforcement Policy.

(NCV 05000446/2016003-01, Failure to Adequately Monitor Feedwater System Check

Valve Performance)

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

On July 7, 2016, the inspectors reviewed a risk assessment and the risk management

actions taken by the licensee in response to elevated risk associated with performing an

oil sample on spent fuel pool pump X-01.

The inspectors verified that this risk assessment was performed timely and in

accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant

procedures. The inspectors reviewed the accuracy and completeness of the licensees

risk assessment and verified that the licensee implemented appropriate risk

management actions based on the result of the assessment.

The inspectors also observed portions of three emergent work activities that had the

potential to affect the functional capability of mitigating systems:

  • August 18, 2016, Unit 2, Steam generator blowdown isolation valve 2-HV-2399

elastomer replacement

turbine driven auxiliary feedwater pumps

  • September 16, 2016, Unit 2, loop A safety chiller emergent maintenance

The inspectors verified that the licensee appropriately developed and followed a work

plan for these activities. The inspectors verified that the licensee took precautions to

minimize the impact of the work activities on unaffected SSCs.

A-10

These activities constituted completion of four maintenance risk assessments and

emergent work control inspection samples, as defined in Inspection Procedure 71111.13.

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments (71111.15)

a. Inspection Scope

The inspectors reviewed seven operability determinations that the licensee performed

for degraded or nonconforming SSCs:

conditioner X-01 partial refrigerant charge

2-01 86-2 lockout relay actuation

auxiliary feedwater pump 1-01 indicating light socket/bulb melted

auxiliary feedwater pump room heat up analyses

pump 2-01 oil leak

generator 2-01 failed KVAR meter

feedwater pumps following identification of an unanalyzed condition

The inspectors reviewed the timeliness and technical adequacy of the licensees

evaluations. Where the licensee determined the degraded SSC to be operable the

inspectors verified that the licensees compensatory measures were appropriate to

provide reasonable assurance of operability. The inspectors verified that the licensee

had considered the effect of other degraded conditions on the operability of the

degraded SSC.

These activities constituted completion of seven operability and functionality review

samples, as defined in Inspection Procedure 71111.15.

b. Findings

No findings were identified.

A-11

1R18 Plant Modifications (71111.18)

.1 Temporary Modifications

a. Inspection Scope

On September 15, 2016, the inspectors reviewed a temporary plant modification to

remove sentinel valves from the turbine driven auxiliary feedwater pumps on Unit 1

and 2.

The inspectors verified that the licensee had installed these temporary modifications in

accordance with technically adequate design documents. The inspectors verified that

these modifications did not adversely impact the operability or availability of affected

SSCs. The inspectors reviewed design documentation and plant procedures affected by

the modifications to verify the licensee maintained configuration control.

These activities constituted completion of one sample of temporary modifications, as

defined in Inspection Procedure 71111.18.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed four post-maintenance testing activities that affected risk-

significant SSCs:

  • April 5, 2016, Unit 1, offsite power supply breaker 1EA2-1 post maintenance test

2-HV-2399 testing following elastomer replacement

following temporary modification

The inspectors reviewed licensing and design-basis documents for the SSCs and the

maintenance and post-maintenance test procedures. The inspectors observed the

performance of the post-maintenance tests to verify that the licensee performed the tests

in accordance with approved procedures, satisfied the established acceptance criteria,

and restored the operability of the affected SSCs.

These activities constituted completion of four post-maintenance testing inspection

samples, as defined in Inspection Procedure 71111.19.

A-12

b. Findings

No findings were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors observed four risk-significant surveillance tests and reviewed test results

to verify that these tests adequately demonstrated that the SSCs were capable of

performing their safety functions:

Other surveillance tests:

  • May 26, 2016, Unit 1, stroke test of power operated relief valve 1-PCV-456
  • August 5, 2016, Unit 2, start and flow test of the turbine driven auxiliary

feedwater pump

  • August 23, 2016, Unit 1, stroke test of containment sump pump discharge line

outside-containment isolation valve 1-HV-5157

  • September 8, 2016, Unit 2, start test of diesel generator 2-01

The inspectors verified that these tests met technical specification requirements, that the

licensee performed the tests in accordance with their procedures, and that the results of

the test satisfied appropriate acceptance criteria. The inspectors verified that the

licensee restored the operability of the affected SSCs following testing.

These activities constituted completion of four surveillance testing inspection samples,

as defined in Inspection Procedure 71111.22.

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation (71114.06)

.1 Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors observed an emergency preparedness drill on September 28, 2016, to

verify the adequacy and capability of the licensees assessment of drill performance.

The inspectors reviewed the drill scenario, observed the drill from the simulator and

emergency operations facility, and attended the post-drill critique. The inspectors

verified that the licensees emergency classifications, off-site notifications, and protective

action recommendations were appropriate and timely. The inspectors verified that any

A-13

emergency preparedness weaknesses were appropriately identified by the licensee in

the post-drill critique and entered into the corrective action program for resolution.

These activities constituted completion of one emergency preparedness drill observation

sample, as defined in Inspection Procedure 71114.06.

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Security

4OA1 Performance Indicator Verification (71151)

.1 Mitigating Systems Performance Index: Emergency AC Power Systems (MS06)

a. Inspection Scope

The inspectors reviewed the licensees mitigating system performance index data for the

period of July 1, 2015 through June 30, 2016 to verify the accuracy and completeness of

the reported data. The inspectors used definitions and guidance contained in Nuclear

Energy Institute Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constituted verification of the mitigating system performance index for

emergency ac power systems for Units 1 and 2, as defined in Inspection

Procedure 71151.

b. Findings

No findings were identified.

.2 Mitigating Systems Performance Index: High Pressure Injection Systems (MS07)

a. Inspection Scope

The inspectors reviewed the licensees mitigating system performance index data for the

period of July 1, 2015 through June 30, 2016 to verify the accuracy and completeness of

the reported data. The inspectors used definitions and guidance contained in Nuclear

Energy Institute Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constituted verification of the mitigating system performance index for

high pressure injection systems for Units 1 and 2, as defined in Inspection

Procedure 71151.

A-14

b. Findings

No findings were identified.

.3 Mitigating Systems Performance Index: Heat Removal Systems (MS08)

a. Inspection Scope

The inspectors reviewed the licensees mitigating system performance index data for the

period of July 1, 2015 through June 30, 2016 to verify the accuracy and completeness of

the reported data. The inspectors used definitions and guidance contained in Nuclear

Energy Institute Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constituted verification of the mitigating system performance index for

heat removal systems for Units 1 and 2, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution (71152)

.1 Routine Review

a. Inspection Scope

Throughout the inspection period, the inspectors performed daily reviews of items

entered into the licensees corrective action program and periodically attended the

licensees condition report screening meetings. The inspectors verified that licensee

personnel were identifying problems at an appropriate threshold and entering these

problems into the corrective action program for resolution. The inspectors verified that

the licensee developed and implemented corrective actions commensurate with the

significance of the problems identified. The inspectors also reviewed the licensees

problem identification and resolution activities during the performance of the other

inspection activities documented in this report.

b. Findings

No findings were identified.

.2 Annual Follow-up of Selected Issues

a. Inspection Scope

The inspectors selected two issues for an in-depth follow-up:

  • During refueling outage 2RF15, October 2015, and refueling outage 1RF18,

May 2016, the licensee credited defense in depth contingency plans, risk

assessments with specified risk management actions, for time periods when the

reactor coolant system would be in a loops not filled condition or when shutdown

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cooling would be in a reduced availability condition due to the increase in risk for

the activities.

The inspectors assessed the licensees risk assessments and the specified risk

management actions. The inspectors identified that the licensee failed to

appropriately manage the risk associated with the activities.

  • On May 18, 2016, after completion of preventative maintenance on the lube oil

cooler for coolant charging pump 1-01, a service water leak was discovered

coming from the cooler head. Upon disassembly, the licensee discovered

significant pitting on the head for the heat exchanger. The licensee initiated

Condition Report 2016-004868 to evaluate the issue, though an operability

evaluation was not performed at the time because the unit was not in a mode of

applicability for the charging pump. The licensee determined that this condition

had been previously identified in Condition Report CR-2014-001804, and parts

were on order to replace the pitted head. The licensees corrective action was to

apply Loctite #2, a sealant material, to stop the leak, noting that this had

previously been evaluated as acceptable in Condition Report CR-2006-001208.

Upon further review inspectors determined that the evaluation performed in CR-

2006-001208 was a one-time evaluation for use of Loctite #2, and did not

establish a basis for the current use. Therefore, an operability evaluation was

required for the subsequent use of Loctite. The licensee initiated Condition

Reports CR-2016-004936 and CR-2016-006674 to address this issue, and

documented a current operability evaluation for use of the Loctite.

Inspectors determined that this issue was a minor violation of Title 10 CFR Part

50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, which

requires, in part, that activities affecting quality shall be accomplished in

accordance with documented instructions, procedures, or drawings, of a type

appropriate to the circumstances. Station Procedure STI-442.01, Operability

Determination and Functionality Assessment Program, is an Appendix B quality

related procedure that is appropriate to the circumstances for evaluating the

operability of safety-related components. Station Procedure STI-442.01 step 6.1,

requires, in part, that when a potential degraded or nonconforming condition is

identified, the shift manager should ensure the operability determination process

is initiated to determine the operability of the structure, system or component.

The inspectors assessed the licensees problem identification threshold, cause

analyses, extent of condition reviews and compensatory actions. The inspectors

verified that the licensee appropriately prioritized the planned corrective actions

and that these actions were adequate to correct the condition.

These activities constituted completion of two annual follow-up sample as defined in

Inspection Procedure 71152.

b. Findings

Introduction. The inspectors identified a Green non-cited violation of

10 CFR 50.65(a)(4), Requirements for Monitoring the Effectiveness of Maintenance at

Nuclear Power Plants, for the licensees failure to adequately manage the increase in

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risk associated with the potential for a loss of decay heat removal during refueling

outages.

Description. During refueling outage 2RF15, October 2015, when the licensee was

setting up for vacuum fill of the reactor coolant system, inspectors reviewed the stations

defense in depth contingency plan 2RF15-01. The inspectors determined that this

contingency plan was a risk assessment with specified risk management actions for

periods when the reactor coolant system would be in a loops not filled condition or

periods of reduced availability of the shutdown cooling system. Inspectors noted that the

contingency plan for these periods of increased risk directed that if residual heat removal

(shutdown cooling) is lost, operators should establish alternate cooling flow path using

Station Procedure ABN-104, Residual Heat Removal System Malfunction, Revision 9,

section 8.

Inspectors reviewed ABN-104, section 8 and noted that it directed operators to start a

safety injection pump in response to a loss of shutdown cooling. Inspectors identified a

concern that the action to start a safety injection pump would occur while in the mode of

applicability for technical specification 3.4.12, Low Temperature Overpressure

Protection System. Technical specification 3.4.12 requires the safety injection pumps

be made incapable of injecting due to concerns of over pressurizing the reactor coolant

system in modes 4, 5, and 6 (the latter only when the reactor vessel head is installed).

The licensee initiated Condition Report CR-2015-009109 to capture the inspectors

concern in the stations corrective action program.

Subsequently, during refueling outage 1RF18, May 2016, inspectors noted that the

licensee again credited a defense in depth contingency plan (1RF18-01) which again

would have operators start a safety injection pump when technical specification 3.4.12

was in effect. During subsequent reviews, the inspectors determined that the licensee

did not have an evaluation for starting a safety injection pump when low temperature

overpressure protection was in effect.

Inspectors determined that the specified risk management action to start a safety

injection pump would restore flow to the core to mitigate the loss of shutdown cooling.

However, the inspectors also determined that the plant is not analyzed for using a safety

injection pump during periods when the reactor coolant system is at low temperatures

requiring low temperature overpressure protection. The proposed use of safety injection

pumps as described in ABN-104, section 8, without analyses for sufficient relief

capability, created the potential for vessel overpressurization and a challenge to the

reactor coolant system barrier. Any challenge to the reactor coolant system barrier

would serve to increase risk. The inspectors also noted that the licensee had several

options to mitigate a potential loss of shutdown cooling that are analyzed during period

where low temperature overpressure protection is required. Specifically, the inspectors

identified that the licensee could start centrifugal charging pumps to restore core flow

following a loss of shutdown cooling. These pumps have slightly less capacity than the

safety inspection pumps which would be bounded by the relief capability required in

technical specification 3.4.12.

Inspectors informed the licensee of the additional concerns and the licensee added them

to Condition Report CR-2015-009109. Inspectors determined that the licensee had not

started a safety injection pump when technical specification 3.4.12 was in effect during

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1RF19 or 2RF18. As corrective actions, the licensee amended Condition Report

CR-2015-009109 to evaluate appropriate risk management actions.

Analyses. The failure to manage the increase in risk associated with the potential for a

loss of decay heat removal during refueling activities is a performance deficiency. The

performance deficiency was more than minor, and therefore a finding, because it was

associated with the procedure quality attribute of the Initiating Events Cornerstone and

affected the cornerstone objective to limit the likelihood of events that upset plant

stability and challenge critical safety functions during shutdown as well as power

operations. Using Inspection Manual Chapter 0609, Appendix K, Maintenance Risk

Assessment and Risk Management Significance Determination Process, dated May 19,

2005, Flowchart 1, Assessment of Risk Deficit, and determined the need to calculate

the risk deficit to determine the significance of this issue. A senior reactor analyst

performed a bounding qualitative assessment, using insights from Inspection Manual

Chapter 0609, Appendix G, Shutdown Operations Significance Determination Process,

and determined the incremental core damage probability deficit was less than 1E-6 and

the incremental large early release probability deficit was less than 1E-7. The influential

assumptions used by the senior reactor analyst included the low exposure time that the

plant is in LTOP conditions, the initiating event frequency associated with a loss of decay

heat removal, available operator mitigation actions that would prevent the use of safety

injection pumps, and the availability of additional equipment to mitigate the loss of decay

heat removal.

In accordance with Flowchart 1 in Appendix K, because incremental core damage

probability deficit was less than 1E-6 and incremental large early release probability

deficit was less than 1E-7, the finding screened as having very low safety significance

(Green). The finding has a human performance cross-cutting aspect associated with

bases for decisions, in that, the licensee failed to ensure that operations leadership

adequately communicate potential problems with the risk management action to start a

safety injection pump when in a mode of applicability for low temperature over pressure

protection [H.10].

Enforcement. Title 10 CFR 50.65(a)(4) requires, in part, that licensees shall assess and

manage the increase in risk that may result from proposed maintenance activities.

Defense in depth contingency plans 2RF15-01 and 1RF18-01 implement pre-planned

risk assessments and specified risk management actions for times during refueling

outages when the reactor coolant system is depressurized and level is lowered.

Contrary to the above, from October 3, 2015, through May 31, 2016, the licensee failed

to manage the increase in risk from proposed maintenance activities. Specifically, the

licensee implemented a risk management action that did not reduce the risk, instead it

called for placing the plant in an unanalyzed condition which could elevate risk. As an

immediate corrective action the licensee initiated Condition Report CR-2015-009109 to

evaluate appropriate risk management actions. Since this violation was of very low

safety significance (Green) and has been entered into the corrective action program as

Condition Report CR-2015-009109, this violation is being treated as a non-cited violation

consistent with Section 2.3.2 of the NRC Enforcement Policy.

(NCV 05000445/2016003-02; 05000446/2016003-02, Failure to Manage Risk During

Refueling Outages)

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4OA5 Other Activities

a. Inspection Scope

The inspectors evaluated the impact of financial conditions on continued safe

performance at Comanche Peak. In that the licensees parent company, Energy Future

Holdings, was under bankruptcy protection/reorganization during the inspection period,

NRC Region IV conducted special reviews of processes at Comanche Peak. The

inspectors evaluated several aspects of the licensees operations to determine whether

the financial condition of the station impacted plant safety. The factors reviewed

included: (1) impact on staffing, (2) corrective maintenance backlog, (3) changes to the

planned maintenance schedule, (4) corrective action program implementation, and

(5) reduction in outage scope, including risk-significant modifications. In particular, the

inspectors verified that licensee personnel continued to identify problems at an

appropriate threshold and enter these problems into the corrective action program for

resolution. The inspectors also verified that the licensee continued to develop and

implement corrective actions commensurate with the significance of the problems

identified.

The special review of processes at Comanche Peak included continuous reviews by the

Resident Inspectors, as well as the specialist-led baseline inspections completed during

the inspection period which are documented previously in this report.

b. Findings

No findings were identified.

4OA6 Meetings, Including Exit

Exit Meeting Summary

On July 7, 2016, the resident inspectors presented the inspection results to Mr. S. Sewell,

Senior Director of Engineering and Regulatory Affairs, and other members of the licensee staff.

The licensee acknowledged the issues presented. The licensee confirmed that any proprietary

information reviewed by the inspectors had been returned or destroyed.

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SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

G. Struble, Manager, Operations/Simulator Training

J. Alldredge, Technician, Radiation Protection

T. Curtis, Lead Environmental Technician

S. Darter, Coordinator, Radiation Protection

S. Dixon, Consulting Licensing Analyst/Regulatory Affairs

T. Emery, Technician, Radiological Environmental Monitoring Program

T. Hope, Manager, Regulatory Affairs

B. Knapp, Acting Manager, Radiation Protection

M. Macho, Supervisor, Radiation Protection

S. Peterson, Senior Calibration Laboratory Technician, Radiation Protection

K. Powell, Supervisor, Radiation Protection

M. Syed, Engineer, Systems Engineer

M. Watkins, Lead Technician, Instruments and Controls Maintenance

J. Barnette, Consultant, Licensing Technologist

S. Bartholomew, Analyst, Emergency Preparedness

G. Bryan, Operations Specialist, Emergency Preparedness

K. Faver, Planner, Emergency Preparedness

R. Fishencord, Planner, Emergency Preparedness

J. Hull, Manager, Emergency Preparedness

R. Marquez, Planner, Emergency Preparedness

S. Sewell, Senior Director of Engineering and Regulatory Affairs

D. Volkening, Manager, Nuclear Oversight

T. McCool, Site Vice President

B. Knowles, Radiation Protection Staff

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

Failure to Adequately Monitor Feedwater System Check Valve

05000446/2016003-01 NCV

Performance (Section 1R12)

05000445/2016003-

Failure to Manage Risk During Refueling Outages (Section

02;05000446/2016003- NCV

4OA2)

02

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LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

Procedures

Number Title Revision

STA-629 Switchyard Control and Transmission Grid Interface 7

Section 1R04: Equipment Alignment

Condition Reports

CR-2016-007245

Drawings

Number Title Revision

E1-0020 125V DC One Line Diagram CP-20

E1-0021 Common Auxiliary Control Fuel and Turbine Buildings Normal CP-22

480VC MCCs One Line Diagram

Procedures

Number Title Revision

SOP-904 Fire Protection Main Water Supply and Fire Pumps System 16

OPT-215 Class 1E Electrical Systems Operability 15

Section 1R05: Fire Protection

Condition Reports

CR-2016-002654

Drawings

Number Title Revision

E1-2020 Safeguard Building Fire Detection Plan EL 773-0, 790-6 and CP-2

800-6

Procedures

Number Title Revision

SAF-104 Inspection of Respiratory Protection Equipment (Maintenance 11

and Repair)

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Procedures

Number Title Revision

ABN-901 Fire Protection System Alarms or Malfunctions 2

FPI-103A Fire Preplan Instruction Manual, Unit 1 Safeguards Building 4

Elevation 810-6, Rad. Pen. Area & Elec. Equip. Rm

Miscellaneous Documents

Number Title Revision

-- Fire Protection Report 30

Work Orders

4789803

Section 1R06: Flood Protection Measures

Calculations

Number Title Revision

SI-CA-0000-693 Miscellaneous Building - Flooding Analysis 1

Section 1R11: Licensed Operator Requalification Program and Licensed Operator

Performance

Procedures

Number Title Revision

EOP-3.0A Steam Generator Tube Rupture 9

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Condition Reports

CR-2016-007272 CR-2016-000493 CR-2016-007720 CR-2016-007428 CR-2016-007690

Procedures

Number Title Revision

DID XPWR-SFP- SFP Cooling During Non-Refueling Outage Conditions -

01

STI-600.01 Protecting Plant Equipment and Sensitive Equipment Controls 1

MSM-GO-0213 Sway Strut Maintenance 1

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Work Orders

5320735 5210636

Section 1R15: Operability Determinations and Functionality Assessments

Calculations

Number Title Revision

1-EB-302-4 As Built HVAC Calculation - Auxiliary Feedwater Pump Room 5

Unit 1

Condition Reports

CR-2016-003089 CR-2016-007251 CR-2016-007653 CR-2016-007840

Work Orders

5010266

Section 1R18: Plant Modifications

Miscellaneous Documents

Number Title Revision

FDA-2016- Create Temp Mod FDA to Remove the Sentinel Valves on the 00

000123-01-00 Casing of the TDAFW Pump Turbines

Work Orders

5330786 5330788

Section 1R19: Post-Maintenance Testing

Condition Reports

CR-2016-000493 CR-2016-007559 TR-2016-004759 CR-2016-005744 CR-2016-005216

CR-2016-003163

Drawings

Number Title Revision

E1-0031-07 6.9 kV Switchgear Bus 1EA2 Breaker 1EA2-2 Schematic CP-13

Diagram

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Procedures

Number Title Revision

MSM-G0-0213 Sway Strut Maintenance 1

MSM-G0-4004 Baker On-line Motor Testing 5

MSM-C0-7310 Service Water Pump Maintenance 5

SOP-603A 6900 V Switchgear 16

MSE-G0-0020 Relay Calibration 5

Work Orders

5210636 5330786 4297555 5008028 4947477

4986918 5008083 5136434 4913385

Section 1R22: Surveillance Testing

Condition Reports

CR-2016-007588

Drawings

Number Title Revision

M2-0206 Flow Diagram Auxiliary Feedwater System CP-15

Procedures

Number Title Revision

OPT-206B AFW System 22

OPT-503A Cntmt Isol Valves ASME Testing 15

Work Orders

5270846

Section 1EP6: Drill Evaluation

Procedures

Number Title Revision

EPP-121 Re-Entry, Recovery and Closeout 10

EPP-116 Emergency Repair & Damage Control and Immediate Entries 9

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Procedures

Number Title Revision

EPP-109 Duties and Responsibilities of the Emergency Coordinator / 15

Recovery Manager

ABN-907 Acts of Nature 15

Section 4OA2: Problem Identification and Resolution

Condition Reports

CR-2006-001208 CR-2014-001804 CR-2016-004868 CR-2016-004936

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