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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20211B1851999-08-16016 August 1999 Forwards Response to 990308 RAI Re Amends to License R-66 & Ts.Proposed Wording for possession-only License & Revised & New Ts,Included ML20211B9041999-08-16016 August 1999 Forwards Substitute Cavalier TS Pages 32 & 33 for NRC Copy of Cavalier TS Amend Application,Replacing Old Page 32 ML20207A4371999-05-24024 May 1999 Forwards Advance Notification of Spent Nuclear Research Reactor Fuel Shipment R66-99-2 from U VA Nuclear Reactor Facility to Savannah River,Sc.Details Concerning Shipment in Attachment.Attachment Withheld ML20217A6321999-05-24024 May 1999 Provides Advance Notification of Spent Nuclear Research Reactor Fuel Shipment R66-99-2 from Univ of Virginia Nuclear Facility to Savannah River,South Carolina.Encl Withheld ML20206K8071999-05-0606 May 1999 Forwards Insp Rept 50-062/99-201 on 990414-16.No Violations Noted.Insp Consisted of Selective Exams of Procedures & Representative Records,Interviews with Personnel & Observations of Activities in Progress ML20205J4271999-03-30030 March 1999 Submits Advanced Notification of Upcoming Spent Nuclear Reactor Fuel Shipment R66-99-1 from Univ of VA Nuclear Reactor Facility to Savannah River,Sc,Per 10CFR73.Details of Shipment,Encl.Without Encl ML20207K2501999-03-0808 March 1999 Forwards Request for Addl Info Re Amend Request for License R-66 Submitted on 980929 ML20203A1331999-02-0303 February 1999 Requests That Senior Reactor Operator License SOP-70161,on Univ of VA Reactor (License R-66) of CA Bly,Be Terminated ML20202B3421999-01-25025 January 1999 Ack Receipt of 990107 Response to Violations Noted in Insp Rept 50-062/98-202.Response Meets Requirements of 10CFR2.201 ML20206P2991999-01-0707 January 1999 Responds to NRC Re Violations Noted in Insp Rept 50-062/98-202.Corrective Actions:Correct Name for Content Matl Being Shipped Is Now Typed Onto All Shipping Forms ML20198L1161998-12-29029 December 1998 Responds to Request for Updated Version of Route Approved by .Enclosure 1 & Page 7 of Enclosure 2 to Be Incorporated with 981026 Package Encl ML20198J2221998-12-21021 December 1998 Forwards Amend 24 to License R-66 & Safety Evaluation.Amend Removes Surveillance Requirements for Rod Drop Measurements & Primary Coolant Flow Calibr ML20198F1101998-12-21021 December 1998 Requests 30-day Extension to Response to NRC Rai, ML20197H6901998-12-10010 December 1998 Submits Clarification of Request for Amend to Univ of VA Reactor TS Dtd 981203.Request Remains Active ML20197H5701998-12-0909 December 1998 Forwards Insp Rept 50-062/98-202 on 981116-19 & Notice of Violation.One Violation Identified.Various Aspects of Operations,Safety & Security Programs Inspected Including Selective Exams of Procedures & Representative Records ML20197G9721998-12-0303 December 1998 Informs That Univ of VA Is in Process of Preparing Response to NRC 981123 RAI Re Proposed Set of UVAR TS Amends Submitted on 980929.Listed Are Two UVAR TS Considerations That Are Being Brought to NRC Attention for Resolution ML20196B1081998-11-23023 November 1998 Forwards Request for Addl Info Re Amend Request for Amended FOL R-66 for University of Virginia Research Reactor, Submitted on 980929.Response Requested within 30 Days of Date of Ltr ML20155D4711998-10-30030 October 1998 Forwards Advance Notification of Spent Nuclear Research Reactor Fuel Shipment R66-98-1 from U VA Nuclear Reactor Facility to Savannah River,Sc.Details of Shipment Are Encl. Without Encl ML20198C8351998-10-30030 October 1998 Forwards Advance Notification of Spent Nuclear Research Reactor Fuel Shipment R66-98-1 from Univ of VA Nuclear Reactor to Savannah River,Sc.Details of Shipment Encl. Without Encl ML20155C1271998-10-27027 October 1998 Informs That Univ of Virginia,Cavalier & UVAR Reactor Operator Requalification Program Meets Requirements of Regulations & Therefore,Acceptable.Implementation of Approved Program Should Begin Immediately ML20155B6031998-10-26026 October 1998 Refers to Request Dtd 980922,for Approval of Route to Be Used for Transport of Spent Fuel from University of Virginia Nuclear Reactor Facility,Charlottesville,Va to Us DOE Savannah River Site,Aiken,Sc ML20154H9561998-10-0707 October 1998 Forwards Response to NRC Request for Addl Info Re Revised Reactor Operator Requalification Program ML20239A1061998-09-0303 September 1998 Forwards RAI Re Revised Reactor Operator Requalification Program,Submitted by Ltr ML20236X8071998-08-0303 August 1998 Forwards Revised Operator Requalification Program for NRC Review & Approval.New Program Takes Into Account de-facto Limitations of Licensed Ro/Sro Duties Just to Fuel Handling Activities,Given That Reactor Core Is Permanently Unloaded ML20236Q9931998-07-15015 July 1998 Withdraws 960319 Request That Revised Security Plan Become License Amend,Per 10CFR50.34 & 10CFR50.59,due to Permanent Shutdown of Univ of VA Reactor,Effective 980701 ML20236K4741998-07-0707 July 1998 Forwards Amend 8 to License R-123 & Safety Evaluation. Amend Tranfers Responsibility for Overall Mgt of CAVALIER from School of Engineering to Office of Vice Provost for Research ML20236F7091998-06-26026 June 1998 Ack Receipt of ,Informing NRC of Univ of Virginia Decision to Cease Operations at Univ of Virginia Research by 980701 & Being Process to Decontaminate & Decommission Facility ML20249C3801998-06-22022 June 1998 Submits Formal Notification to Us NRC of Intention of Univ of VA to Begin Process That Will Lead to Decontamination & Decommissioning of Univ of VA Reactor Covered by License R-66 ML20249B8641998-06-18018 June 1998 Submits Response to NRC RAI Re TS Amend Request ML20249A5921998-06-15015 June 1998 Forwards Amend 23 to License R-66 & Safety Evaluation.Amend Transfers Responsibility for Overall Mgt of University of Virginia Research Reactor from School of Engineering to Ofc of Vice Provost for Reseach IR 05000062/19982011998-05-0404 May 1998 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-062/98-201.NRC Will Examine Implementation of Corrective Actions During Future Insp ML20217H7921998-04-23023 April 1998 Informs That Univ of VA Administration Had Made Decision to Move Toward Ceasing Operations of UVAR Reactor,As Stated in ML20217H7891998-04-15015 April 1998 Accepts Ltr as Official Notification to NRC of Univ of VA Intent to Decommission Univ of UVAR Reactor ML20216B6331998-04-0606 April 1998 Submits Answer to NRC Request for Addl Info Re Univ of VA Reactor UVAR & Univ VA Cavalier ML20217M1531998-04-0101 April 1998 Responds to NRC Re Violations Noted in Insp Repts 50-062/98-201 & 50-396/98-201 on 980126-28.Corrective Actions:Held make-up Evacuation Drill & Tested Evacuation Alarm.Greater Attention in Documenting & Filing Paperwork ML20217G6241998-03-30030 March 1998 Forwards Annual Rept of Operations of Univ of VA Reactor & Cavalier Reactor During Period 970101-1231,per Section 6.7.2 of TS ML20216G8581998-03-11011 March 1998 Forwards Request for Addl Info Re Review of Amend Request for License R-66,submitted on 980226.Responses Requested to Be Provided within 60 Days of Date of Ltr ML20197B7881998-03-0404 March 1998 Forwards Insp Rept 50-062/98-201 on 980126-28 & Notices of Violation & Deviation.Various Aspects of Radiation Protection & Safety Programs Were Inspected ML20203L9351998-02-18018 February 1998 Forwards Copy of Results of Operator Initial Exam Conducted at Univ of Virginia on 980115-16 ML20197F7171997-12-11011 December 1997 Forwards Insp Repts 50-062/97-201 & 50-396/97-201 on 971111- 13.No Violations Noted ML20197G1381997-12-11011 December 1997 Responds to Electronic Mail Message of 971201 Re Comparative Costs of Relicensing & Decommissioning non-power Reactors ML20198Q3541997-11-0303 November 1997 Confirms Arrangements P Isaac Made W/P Benneche for Administration of Operator Licensing Exams at Univ of Virginia Reactor.Exams Scheduled for Wk of 980112.Requests Ref Matl Listed in Encls ML20198F6671997-08-0101 August 1997 Informs That on 970804,non-power Reactor Insp Program Will Be Transferred from Region II Ofc to NRR ML20141K6131997-05-15015 May 1997 Forwards Insp Rept 50-062/97-01 on 970414-17.No Violations Noted ML20138H0911997-05-0707 May 1997 Forwards Scenerio for 961119 Emergency Drill IR 05000062/19960031997-04-22022 April 1997 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-062/96-03. Corrective Actions Will Be Examined During Future Insp ML20137V9121997-03-25025 March 1997 Forwards List of Phone Numbers & Directions to NRC Region II Ofc.Ofc Will Move to Atlanta Federal Center Complex on 970425.During Transition Period of 970425-27 Ofc Will Not Be Open for Business ML20137U9911997-03-18018 March 1997 Forwards Annual Rept of Operations of Univ of VA Reactor & Cavalier Reactor for Period 960101-1231.W/o Encl ML20141K4911997-02-17017 February 1997 Forwards Response to Violations Noted in Insp Rept 50-062/96-03.Corrective Actions:Reactor Staff Will Request Approval from Univ of VA Reactor Safety Committee for Changes to UVAR Emergency Plan & Implementing Procedures ML20133F8671996-12-20020 December 1996 Forwards Insp Rept 50-062/96-03 on 961118-21.No Violations or Deviations Noted 1999-08-16
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20211B1851999-08-16016 August 1999 Forwards Response to 990308 RAI Re Amends to License R-66 & Ts.Proposed Wording for possession-only License & Revised & New Ts,Included ML20211B9041999-08-16016 August 1999 Forwards Substitute Cavalier TS Pages 32 & 33 for NRC Copy of Cavalier TS Amend Application,Replacing Old Page 32 ML20217A6321999-05-24024 May 1999 Provides Advance Notification of Spent Nuclear Research Reactor Fuel Shipment R66-99-2 from Univ of Virginia Nuclear Facility to Savannah River,South Carolina.Encl Withheld ML20207A4371999-05-24024 May 1999 Forwards Advance Notification of Spent Nuclear Research Reactor Fuel Shipment R66-99-2 from U VA Nuclear Reactor Facility to Savannah River,Sc.Details Concerning Shipment in Attachment.Attachment Withheld ML20205J4271999-03-30030 March 1999 Submits Advanced Notification of Upcoming Spent Nuclear Reactor Fuel Shipment R66-99-1 from Univ of VA Nuclear Reactor Facility to Savannah River,Sc,Per 10CFR73.Details of Shipment,Encl.Without Encl ML20203A1331999-02-0303 February 1999 Requests That Senior Reactor Operator License SOP-70161,on Univ of VA Reactor (License R-66) of CA Bly,Be Terminated ML20206P2991999-01-0707 January 1999 Responds to NRC Re Violations Noted in Insp Rept 50-062/98-202.Corrective Actions:Correct Name for Content Matl Being Shipped Is Now Typed Onto All Shipping Forms ML20198F1101998-12-21021 December 1998 Requests 30-day Extension to Response to NRC Rai, ML20197H6901998-12-10010 December 1998 Submits Clarification of Request for Amend to Univ of VA Reactor TS Dtd 981203.Request Remains Active ML20197G9721998-12-0303 December 1998 Informs That Univ of VA Is in Process of Preparing Response to NRC 981123 RAI Re Proposed Set of UVAR TS Amends Submitted on 980929.Listed Are Two UVAR TS Considerations That Are Being Brought to NRC Attention for Resolution ML20198C8351998-10-30030 October 1998 Forwards Advance Notification of Spent Nuclear Research Reactor Fuel Shipment R66-98-1 from Univ of VA Nuclear Reactor to Savannah River,Sc.Details of Shipment Encl. Without Encl ML20155D4711998-10-30030 October 1998 Forwards Advance Notification of Spent Nuclear Research Reactor Fuel Shipment R66-98-1 from U VA Nuclear Reactor Facility to Savannah River,Sc.Details of Shipment Are Encl. Without Encl ML20154H9561998-10-0707 October 1998 Forwards Response to NRC Request for Addl Info Re Revised Reactor Operator Requalification Program ML20236X8071998-08-0303 August 1998 Forwards Revised Operator Requalification Program for NRC Review & Approval.New Program Takes Into Account de-facto Limitations of Licensed Ro/Sro Duties Just to Fuel Handling Activities,Given That Reactor Core Is Permanently Unloaded ML20236Q9931998-07-15015 July 1998 Withdraws 960319 Request That Revised Security Plan Become License Amend,Per 10CFR50.34 & 10CFR50.59,due to Permanent Shutdown of Univ of VA Reactor,Effective 980701 ML20249C3801998-06-22022 June 1998 Submits Formal Notification to Us NRC of Intention of Univ of VA to Begin Process That Will Lead to Decontamination & Decommissioning of Univ of VA Reactor Covered by License R-66 ML20249B8641998-06-18018 June 1998 Submits Response to NRC RAI Re TS Amend Request ML20217H7921998-04-23023 April 1998 Informs That Univ of VA Administration Had Made Decision to Move Toward Ceasing Operations of UVAR Reactor,As Stated in ML20217H7891998-04-15015 April 1998 Accepts Ltr as Official Notification to NRC of Univ of VA Intent to Decommission Univ of UVAR Reactor ML20216B6331998-04-0606 April 1998 Submits Answer to NRC Request for Addl Info Re Univ of VA Reactor UVAR & Univ VA Cavalier ML20217M1531998-04-0101 April 1998 Responds to NRC Re Violations Noted in Insp Repts 50-062/98-201 & 50-396/98-201 on 980126-28.Corrective Actions:Held make-up Evacuation Drill & Tested Evacuation Alarm.Greater Attention in Documenting & Filing Paperwork ML20217G6241998-03-30030 March 1998 Forwards Annual Rept of Operations of Univ of VA Reactor & Cavalier Reactor During Period 970101-1231,per Section 6.7.2 of TS ML20138H0911997-05-0707 May 1997 Forwards Scenerio for 961119 Emergency Drill ML20137U9911997-03-18018 March 1997 Forwards Annual Rept of Operations of Univ of VA Reactor & Cavalier Reactor for Period 960101-1231.W/o Encl ML20141K4911997-02-17017 February 1997 Forwards Response to Violations Noted in Insp Rept 50-062/96-03.Corrective Actions:Reactor Staff Will Request Approval from Univ of VA Reactor Safety Committee for Changes to UVAR Emergency Plan & Implementing Procedures ML20132F5931996-12-16016 December 1996 Responds to 960919 RAI Re TS Amend Request . Withdrawal of Proposed TS Amend,Requested ML20134L0571996-11-15015 November 1996 Requests 30 Day Extension for Response to NRC 960919 RAI Re 960528 Application for Amend to License R-66 ML20128N1421996-10-11011 October 1996 Requests Extension to 961119 Re Submittal of TS Amend RAI ML20117J2161996-05-28028 May 1996 Forwards Proposed TS Amend,Consisting of Revised (or Deleted) Definitions for Terms Reactor Secured,Reactor Shutdown,Reactor Operating,Reference Core Condition & Reactivity Limits ML20106J9561996-03-26026 March 1996 Forwards Public Version of Revised Epips,Including Rev 19 to EPIP-6 & Rev 19 to EPIP-14 ML20101N8651996-03-26026 March 1996 Forwards Rev 19 to EPIPs for Facility,Including EPIP 6,page 2,EPIP 6,Attachment 1,pages 1 & 2 & EPIP 14,Attachment 1, Page 1.Rev Reflects Changes in Personnel & Phone Numbers.W/O Encls ML20101E3891996-03-19019 March 1996 Forwards Proprietary Amendment to License R-66 Re Security Plan for Univ of VA Reactor Facility.Encl Withheld (Ref 10CFR2.790) ML20100K6001996-02-22022 February 1996 Forwards Revised Version of Reactor Facility Security Plan. Encl Withheld ML20094C4081995-10-26026 October 1995 Forwards Revised Pages to SAR & New Proposed TS 4.9, Surveillance of Activity in Secondary Coolant Sys, in Response to NRC 951025 RAI ML20093L1041995-10-19019 October 1995 Forwards NRC Questionaire & Licensee Answers Re Proposed Amend to SAR of 951010,including Proposed SAR Section 9.20.8 as Component of Response to NRC Question 6. Replacement of Proposed SAR Amend Also Encl ML20095F2681995-10-11011 October 1995 Forwards Univ of VA Nuclear Reactor Facility 1995 Annual Emergency Preparedness Drill Scenario.Requests That Encl of Ltr Be Held from NRC Public Document Room Until After Drill Event ML20093C7411995-10-10010 October 1995 Forwards SAR for Low-Enriched U Fueled Univ of VA Reactor ML20083P7031995-05-11011 May 1995 Advises That All HEU Fuel Elements Removed from Facility & Condition II.B.(4) Can Be Deleted from License R-66,in Response to NRC 950508 RAI Re Proposed Changes to License. Licensee Still Possesses HEU in Form of Fission Chambers ML20097J3921995-04-20020 April 1995 Forwards Response to NRC 950309 RAI Re Proposed Changes to Ts.Revised TS Also Encl ML20082N9141995-04-19019 April 1995 Forwards Estimated Uncertainity for Univ of VA Reactor Reactivity Measurements ML20081L9751995-03-27027 March 1995 Forwards Rev 18 to EPIPs & Rev 3 to Emergency Plan ML20078C7201994-10-26026 October 1994 Requests That NRC Take No Further Action on Review of Security Plan Proposed by Licensee on 900713,in View of Completed Conversion of Univ of VA Reactor to LEU Fuel & Upcoming Decommissioning of 100W Cavalier Reactor ML20077C3841994-10-18018 October 1994 Forwards Univ of VA Nuclear Reactor Facility 1994 Emergency Preparedness Drill Scenario for 941122 ML20076F9031994-10-13013 October 1994 Forwards HEU to LEU Fuel Conversion Rept, as Required by Attachment to Amend 20,License R-66 ML20077S3361994-07-29029 July 1994 Submits Affidavit Re NRC Request for Publication of Proprietary & Confidential Info of Protechnics Intl,Inc,In Connection W/Spill Which Took Place at Univ of VA Reactor Facility in 1992 & Reported to NRC by Univ on 920911 ML20070G2781994-07-13013 July 1994 Responds to NRC Re Violations Noted in Insp Rept 50-062/94-04.Corrective Action:Many Routine Surveys Performed ML20063F9101994-01-14014 January 1994 Forwards Rev 16 to Epips.Requests Ack Receipt & Filing of Rev by Returning Completed Cover Sheet.W/O Encl ML20062N6471994-01-10010 January 1994 Informs That Rd Flack Named Dept Chairman,Effective 931201 ML20059K0121993-11-0404 November 1993 Informs Nrc,Rd Flack,Named Acting Chair of Dept of Mechanical,Aerospace & Nuclear Engineering by Dean of School of Engineering & Applied Science ML20056F7791993-08-26026 August 1993 Responds to NRC Re Violations Noted in Insp Rept 50-062/93-01.Corrective Actions:Complete Review of Console Schematics & Electronics Performed & Improved Labelling Sys Adopted for Modules in Console 1999-08-16
[Table view] |
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SCH00L OF ENG 9EERING $
October 10,'1995 &APPLIEDSCIENCE NUCLEAR REACTOR FACILITY Document Control Desk Department of Mechanical, U.S. Nuclear Regulatory Commission Aerospace & Nudear Engineering Washington, D.C. university or virginia Charlottesvide, VA 22903-2442 20555 804-982-5440 FAX: 804-982-5473
Subject:
Amendment to the Safety Analysis Report (SAR) for the University of Virginia Reactor (UVAR), Docket No. 50-62, License R-66, pertaining to its Heat Exchanger.
. Gentlemen:
In August 1995, the University of Virginia Reactor staff performed maintenance on the non-radioactive secondaiy side of the UVAR heat exchanger. Secondary water carries heat from the reactor to the environment by way of an outdoor cooling tower. Due to secondary coolant contact with the environment, maintenance involving cleaning of biological fouling in the tubes is done from time to time. While performing this cleaning, accumulated scale was noted on the ends of some tubes at the tube sheet. This scale was removed and samples sent for analysis by the commercial provider of secondary water corrosion inhibiting chemicals.
Following the cleaning of the heat exchanger, the UVAR was operated for a brief time until a small heat exchanger leak was discovered. It was noted that, depending on the on/off status of the primary and secondary pumps, the leak would go from the secondary to the primary side and vice-versa. Throughout this period, poolwater quality was monitored and maintained within technical specification limits, and secondary water radioisotope concentrations levels were determined to have been low and not to have )
exceeded off-site release limita. Currently, the heat exchanger has been valved off and the UVAR only is available for low power operation in natural circulation mode.
This submittal contains a request for an amendment to the UVAR license, to permit the staff to install mechanical expanding plugs in secondary-side heat exchanger tubes which leak (at present, four out of 712). Please find in attachment a safety analysis performed by the University of Virginia (U.Va.) with reference to the repair, and eventual replacement, of the UVAR heat exchanger. We propose that the UVAR LEU Safety Analysis Report be amended by the addition or replacement of the following:
Table of Contents for UVAR LEU SAR (revised)
Figure 4.1, pg 4-4: Cooling System Flow Diagram (updated)
Section 4.6.1., pg 4-7-A: Replacement of Heat Exchanger System Components (new)
Sections 4.7 and 4.8, pg 4-7-B (reformatted)
Table 4.1, pg 4-8: Current Heat Exchanger Specifications (updated)
Table 4.1.A., pg 4-8-A: Heat Exchanger Secondary Tube Plug Specification (new)
Section 9.19, pg 9 73..: Heat Exchanger Secondary Tube Plugging Analysis (new) l Section 9.20, pg 9-77..: Heat Exchanger Primary-to-Secondary Leak Analysis (new)
)
Section 9.21, pg 9-87..: Heat Exchanger Secondary to-Primary Leak Analysis (new) l
....,,n .
9510130007 951010 PDR OI P
ADOCK 05000062 .<
.PDR. 1 I
I (UVAR SAR Amendment, page 2, cont.)
Also included in this submittal is a report describing the events surrounding the discovery and the proposed repair of the small heat exchanger leak.
The analysis of "unreviewed safety questions" is required by 10CFR50.59, as a precondition to obtaining authorization from the U.Va. Reactor Safety Committee, and from the Nuclear Regulator Commission, for the plugging of several tubes in the heat exchanger and a return to full power operation. On October 9,1995 the U.Va. Reactor Safety Committee reviewed and approved this safety analysis as well as new or revised procedures for annual heat exchanger inspections, increased secondary water monitoring frequency, actions to be taken in the event of heat exchanger leaks, and heat exchanger repair. Historically, the impact of heat exchanger leaks has not been analyzed for research reactors. As determined in our safety analysis, realistic short-term leaks of l reactor pool water through the heat exchanger to the environment are of negligible
. impact. Moreover, these leaks are, of course, bounded by the analyzed survivable design-basis accident scenario involving loss of all poolwater.
Mindful of the needs of its faculty and reactor users, and in view of the benign results of the analysis and the simple heat exchanger repair, U.Va. is requesting an expedited review and approval of the SAR amendment from the NRC, as well as an early authorization to repair the heat exchanger and return the UVAR to full power operation.
The return of the reactor to forced circulation operating mode will help prevent !
potentially corrosive effects of stagnant water in the primary and secondary systems. l Following the repair of the UVAR heat exchanger, the surveillance regime over primary system water quality and radioisotope concentration levels in the secondary system water will be increased to assure that the repair has been successful, and to identify future leaks at an early stage, were they to occur. The enhanced surveillance regime will provide reasonable assurance that there will be no effluent releases above regulatory limits, and that the health and safety of the public will not be endangereq'.
Mj/ County of fh ed Commonwealth ci Wrginia gj ,
i hacby certify that the attached document is a true and l
' exact copy of a -, presented before l
@ o,p. e. om en Robert U. Mulder, Director me th.is g4 c3y g [), ) . , 7 .,,19 @
U.Va. Reactor Facility &
Assoc. Prof. of Nuclear Eng. by hd NId (name of person sechnig ajanspecgenner4 e f % 1, s
(/ . ( f1/
I
' Notary PutM cc: Mr. Craig Basset, NRC Region II, Atlanta, GAMY commission expires 9 19 N -
Mr. Alexander Adams, Jr., NRC Headquarters, Rockville, MD
4 A Report of the lleat Exchanger Leak Discovery on August 22,1995 The following chronology outlines events leading to the generation and discovery of a heat exchanger leak.
i 1. March 1995: Analysis by the Nalco Chemical Company and visual inspection of aluminum test coupons taken from the secondary cooling system in January 1995
, show, for the first time, slight scaling and a slightly elevated corrosion rate compared j to past examinations.
- 2. Aug. 7,1995: The secondary side of the heat exchanger had last been opened in October 1987. In view of the test coupon analysis and this long period since the previous inspection the heat exchanger was opened in August 1995 to examine the tubes and to clean them, as necessary. Scaling was noted on the tube sheets, primarily on the intake sides on both ends and just inside the beginning of many of the tubes near to the point where they are swsged to the tube sheet. Only minor scaling was observed in the tubes past the point where they are held by the tube sheet. No fouling by biological scum was noted.
i
- 3. Aug. 7-14,1995: The insides of heat exchanger tubes were flushed out with clean water and scale was removed to the extent possible. The local service representative from Nalco Chemical Company and her supervisor visit the building (on August 9) i to examine the condition of the heat exchanger and begin the process of trying to determine why the corrosion and scale inhibiting chemicals used in the secondary water did not prevent the scaling observed.
- 4. Aug.15,1995: Prior to closing the secondary side of the heat exchanger, the slight stream of water seen coming out was sampled for radionuclide analysis. The large
~; amount of water which had been used in the cleaning process was believed to be the source of this water. At this time there was full static pressure on the primary side,
- about 24 feet of water, and atmospheric pressure on the secondary side which had been drained. Analysis results obtained on August 16 showed tritium to be present in the leaking water at about the same concentration that it exists in the pool.
The heat exchanger was closed on August 15, the secondaiy side refilled and the secondary pump was turned on in the expectation that a positive pressure differential from secondaiy to primary would stop or reverse the leak. Pool water began to be checked for evidence (change in water quality or other indication) of a secondary to primary leak.
- 5. Aug.16,1995: The first indirect indication of a possible secondary to primary leak 4 is derived from the obseivation that the pool water level, monitored every normal workday, did not slightly drop overnight as is expected from evaporation and
- demineralizer pump shaft seal losses.
1 J
- 6. Aug.17,1995: Reactor was operated at powers up to 2MW for about seven hours.
Pool water samples were taken for analysis. These were analyzed over the next day by gamma spectroscopy and molybdenum-99 from the activation of a molybdenum compound used as a corrosion inhibitor in the secondary water was seen. This verified that a small secondary to primary leak truly existed. An increase in the pool water conductivity at a faster than normal rate supported this conclusion. The water quality was better than the minimum Technical Specification limits (conductivity <
5 pmho/cm). Since the leak was obseived to be into the pool extra samples of the secondary system water were not taken until the normal sampling on August 22.
- 7. Aug.18,1995: Reactor was operated at powers up to 2MW for about 7.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.
Changes in reactor pool water quality (conductivity goes from 1.4 to 2.2 pmho/cm) indicate a continuing secondary to primary leak.
- 8. Aug. 22,1995: Reactor was operated at powers up to 2MW for about seven hours.
Near the end of the operation the monthly water sample from the cooling tower was taken.
4 Sample analysis showed low levels of sodium-24 (~8.8x10 Ci/ml). During reactor operation sodium 24 is normally the most abundant isotope seen in the reactor pool (typically in the range of 104 to 104 yCi/ml) but it is not seen in the cooling tower water. Its presence was evidence of a primary to secondary leak. This was surprising since it was assumed that there was always sufficient differential pressure between the primary and secondaiy sides of the heat exchanger to force leaks from the secondary to the primary side. It was subsequently observed that with the reactor primary pump on, the secondary pump on, and the secondary-side discharge throttle valves to the cooling tower in their current positions, the primary side pressure was somewhat larger than the secondary pressure, making a primary to secondary leak possible. Under other conditions, any leakage is from secondary to primary.
The primary coolant isolation valves were closed approximately 45 minutes after the leak was identified, and UVAR operation restricted to natural convection cooling mode until reviews, approvals and fixes were implemented. The measured concentrations ofidentified radionuclides in the cooling tower water remained below the effluent concentration limits in 10CFR20.
- 9. Aug. 23,1995: Secondary system isolation valve (isolating water in the lower basin of the cooling tower from the heat exchanger) was closed and the secondary water in the heat exchanger and on the downstream side of the isolation valve was drained to the liquid radioactive water tanks. The heat exchanger secondaiy side was re-opened. Upon close inspection two leaking tubes were identified. Two additional leaking tubes, with a much smaller leak rate, were found later. Scale was again obseived located where it had been cleaned off just two weeks earlier.
2
. . _ _ . . . ._ _ m.._. _ . . . . . ~ _ . _ _ _ _ .,_.._.__,..,.._._..-..___..mm_ . _ _ _ _ .
- 10. Aug. 23 - to date: The situation and possible licensee options were discussed with NRC and NIST personnel. NIST provided suggestions for a type of plug design i ideally suited to the UVAR's aluminum heat exchanger. In preparation for the future, and to assess feasibility, rubber tubing, stainless steel bolts and nuts were
. ordered. Plugs were then made and pressure tested in a tube similar to those in the heat exchanger. Reactor operation continues, but restricted to 200 kW in natural convection mode only. This is permitted by Technical Specifications and Standard Operating Procedures (SOP).
i 1
4 3
I Maintenance and Upgrade Actions Being Instituted Plug Leaking Tubes
- 1. Currently four heat exchanger tubes (out of 712) have been identified as leakers.
- . These tubes can be plugged at both ends. Then, leakage through the tubes is
impossible. Pressure fittings plugs of a simple design can be used. The system will !
not " challenge" the plugs in terms of pressure, vibration or radiation levels. The plug l design has been used successfully in a more challenging environment at the National Institutes cf Standards and Technology's NBS Reactor. The plugs can be removed l in the future, if desired. The installation does not affect nearby tubes in any manner. )
1
- 2. A Method has been written to provide direction for the assembly, testing and i installation of plugs in secondary side heat exchanger tubes that have been identified ;
, as leaking. This method is titled " Assembly, Testing and Installation of Plugs m Secondary Side Heat Exchanger Tubes". l l
l l
Procedural Changes
- 1. A new Standard Operating Procedure (SOP) titled " Actions to be Taken in the Event ,
of a Suspected Heat Exchanger Tube Leak" has been approved by the U.Va. Reactor i Safety Committee (ReSC) and will be added as procedure 11.W. to the UVAR SOP Chapter 11 which deals with abnormal conditions. This procedure outlines the symptoms of a possible tube leak, methods to verify whether or not a leak actually i exits and remedial actions to take in order to limit the effects of any leak.
- 2. The current SOP 10.4.G. has been modified (and approved by the ReSC) to increase the frequency of secondary water sampling and analysis by gamma-ray spectroscopy from monthly to weekly.
- 3. A new maintenance procedure has been approved by the ReSC for addition to the SOP as Section 7.15: " Heat Exchanger", to provide for the annual inspection of secondaiy side of the heat exchanger to check for corrosion, scale buildup, fouling and plug integrity. Previously, there was no established frequency for this maintenance item (nor have there been any plugs to check in the past).
Additional Methods The current method, " Cleaning Cooling Tower and Heat Exchanger", has been modified to preclude the removal of scale found inside the secondary tubes. The removal of this scale can induce leaks so it is considered prudent to leave any scale in place, although this might lead to somewhat enhanced corrosion near the site of the scale. Several other improvements to this method have been instituted.
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