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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20217L9371999-10-20020 October 1999 Safety Evaluation Supporting Licensee Proposed Alternative from Certain Requirements of ASME Code,Section XI for First 10-Yr Interval Request for Relief for Containment Inservice Insp Program ML20136F5831995-01-20020 January 1995 Safety Evaluation Re Evaluation of Licensee Response to GL-87-02 ML20154P2621988-09-0202 September 1988 Safety Evaluation Re Response to Generic Ltr 83-28,Item 2.1, (Part 2) Re Vendor Interface Program (Reactor Trip Sys Components).Program Meets Requirements of Item 2.1 (Part 2) of Generic Ltr 83-28 ML20129A9021984-08-24024 August 1984 Safety Evaluation Supporting Amends 105 & 99 to Licenses DPR-31 & DPR-41,respectively IA-84-930, Safety Evaluation Supporting Amends 105 & 99 to Licenses DPR-31 & DPR-41,respectively1984-08-24024 August 1984 Safety Evaluation Supporting Amends 105 & 99 to Licenses DPR-31 & DPR-41,respectively ML20062C4791978-10-25025 October 1978 Safety Eval Supporting Amend 40 & 32 to Lic DPR-31 & DPR-41. Concludes That No Adverse Effects Will Result ML20062C7561978-10-16016 October 1978 Safety Eval Rept Supporting Amend 39 to License DPR-31 ML20062C6961978-09-22022 September 1978 Safety Evaluation Supporting Amend 38 & 31 to Lic DPR-31 & DPR-41.Concludes That No Harm Will Ensue 1999-10-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L9371999-10-20020 October 1999 Safety Evaluation Supporting Licensee Proposed Alternative from Certain Requirements of ASME Code,Section XI for First 10-Yr Interval Request for Relief for Containment Inservice Insp Program ML17355A4471999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Turkey Point,Units 3 & 4.With 991008 Ltr ML17355A4121999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Turkey Point,Units 3 & 4.With 990909 Ltr ML17355A3981999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Turkey Point,Units 3 & 4.With 990809 Ltr ML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17355A3611999-06-30030 June 1999 Refueling Outage ISI Rept. ML17355A3681999-06-30030 June 1999 Revised Update to Topical QA Rept, Dtd June 1999 ML17355A3841999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Turkey Point,Units 3 & 4.With 990713 Ltr ML17355A3511999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Turkey Point,Units 3 & 4.With 990609 Ltr ML17355A3331999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Turkey Point,Units 3 & 4.With 990511 Ltr ML20217B9871999-04-0808 April 1999 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 971014-990408 ML17355A2881999-04-0505 April 1999 COLR for Turkey Point Unit 4 Cycle 18. ML17355A2911999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Turkey Point,Units 3 & 4.With 990414 Ltr ML17355A2551999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Turkey Point Nuclear Power Plant,Units 3 & 4.With 990315 Ltr ML17355A2261999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Turkey Point,Units 3 & 4.With 990211 Ltr ML17355A2201999-01-20020 January 1999 Refueling Outage ISI Rept. ML17355A1911998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Turkey Point,Units 3 & 4.With 990112 Ltr ML18008A0461998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Turkey Point,Units 3 & 4.With 981209 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1891998-11-0909 November 1998 Simulatory Certification Update 2. ML17354B1901998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Turkey Point,Units 3 & 4.With 981112 Ltr 05000250/LER-1998-006-02, :on 981006,unescorted Access Was Granted to Contractor Employee Who Falsified Background Info.Caused by Individual Who Knowingly Provided False Info.Denied Access to Individual on 981006.With1998-10-27027 October 1998
- on 981006,unescorted Access Was Granted to Contractor Employee Who Falsified Background Info.Caused by Individual Who Knowingly Provided False Info.Denied Access to Individual on 981006.With
ML17354B1591998-10-23023 October 1998 COLR for Turkey Point Unit 3 Cycle 17. 05000250/LER-1998-005-02, :on 980924,suspended Safeguards During Severe Weather Due to Personnel Safety.Caused by Severe Weather Associated with Effects of Hurricane Georges.Fully Instituted Compensatory Measure.With1998-10-16016 October 1998
- on 980924,suspended Safeguards During Severe Weather Due to Personnel Safety.Caused by Severe Weather Associated with Effects of Hurricane Georges.Fully Instituted Compensatory Measure.With
ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B1311998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Turkey Point Unit 3 & 4.With 981012 Ltr ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML17354B0981998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Turkey Points,Units 3 & 4.With 980915 Ltr ML17354B0771998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Turkey Point,Units 3 & 4.W/980810 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354B0241998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Turkey Point,Units 3 & 4.W/980709 Ltr ML17354B0171998-06-29029 June 1998 Rev 1 to PTN-FPER-97-013, Evaluation of Turbine Lube Oil Fire. ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML17354A9711998-05-31031 May 1998 Monthly Operating Repts for Turkey Point,Units 3 & 4. W/980611 Ltr ML17354A9231998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Turkey Point,Units 3 & 4.W/980511 Ltr ML17354A8821998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Turkey Point,Units 3 & 4.W/980409 Ltr ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354B0001998-03-18018 March 1998 Florida Power & Light Topical Quality Asurance Rept, Dtd June 1998 ML17354A8311998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Turkey Point,Units 3 & 4.W/980311 Ltr ML17354A7871998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Turkey Point,Units 3 & 4.W/980209 Ltr ML17354A7581997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Turkey Point,Unit 3 & 4.W/980112 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A7381997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Turkey Point,Units 3 & 4.W/971215 Ltr ML17354A7211997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Turkey Point,Units 3 & 4.W/971114 Ltr ML17354A7491997-10-13013 October 1997 SG Insp Rept. ML17354A8851997-10-13013 October 1997 FPL Units 3 & 4 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 960408-971013. ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr 1999-09-30
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NUCLEAR REGULATORY COMMISSION UNITED STATES
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E WASHINGTON, D. C. 20555 i
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I SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION I
j SUPPORTING AMEN 0 MENT NOS.40 AND 32 TO LICENSE NOS. OPR-31 AND DPR-41 I
FLO'1IDA POWER AND LIGHT COMPANY t
TURKEY POINT NUCLEAR GENERATING UNITS NOS. 3 AND 4 2
DOCKET NOS. 50-250 AND 50-251
!O tatroductica By letter dated December 15, 1977, Florida Power and Light Company Ithe licensee) requested amendment of the Technical Specifications appended to Facility Operating License Nos. DPR-31 and DPR-41 for the Turkey Point Plant Unit Nos. 3 and 4 The amendment reduces the maximum pressurizer heatup rate fran 200*F per hour to 100*F per hour.
Backcround In August 1977, Mitsubishi Heavy Industries, Ltd. of Japan noted an inconsistency in the pressurizer heatup rate stated in their Technical Speci fications.
Specification 3.4.9 required a heatup rate of 200*F/hr; Specification 5.7.1, however, recuired a heatup rate of 100*F/hr.
This discrepancy was reported to the Westinghouse Electric Corporation (Westinghouse), who then reviewed their analysis of the pressurizer heatup O
rate and dete=iaed that the correct heatuP rate is 100 F/hr, and that the correct cocidown rate is 200*F/hr; the Technical Specifications for Turkey Point stated that pressurizer heatup and cooldewn rates were 200*F/hr.
Westinghouse then notified the Nuclear Regulatory Commission (the Commission) and the licensee of this problem.
The licensee reported the error as Report-able Occurrences 50-250/77-7 and 50-251/77-7.
The requested amendment would correct the error in the pressurizer heatup rate limit.
Evaluation In designing the pressurizer, Westinghouse perfonned a thennal stress analysis which analyzed the fatigue resulting fran a heatup rate of 100*F/hr and a cool-down rate of 200*F/hr.
This analysis meets the standards of the ASME Code,Section III, which requires that the analysis be b4 sed on a usage factor.
The usage factor represent the fraction of the fatigue life (the total amount amount of stress that a particular component is desianed to handle), with a usage factor of zero implying that no stress has been exerted on the comconent, and a usage factor of one implying that the stress exerted on the complying that the stress exerted on the component is equal to the amount of stress 78//@#z/
9
that the camponent is designed to handle.
For any piece of equipment, certain canponents receive more stress than others.
For the pressurizer, this canponent is the surge nozzle, which has i
a usage factor of 0.9 for the design numbers listed above. This usage factor is such that if the heatup and cooldown rates used in the analysis were exceeded more than a few times, the actual usage factor for the surge nozzle would exceeo 1.0, which is not allowable under the ASME Code. Thus, we conclude that reducing the heatup rate limit from 200*F/hr to 100*F/hr is necessary to maintain themal stresses in the pressurizer to allowable levels.
For the same reasons, we further conclude that the cooldown rate limit presently listed in the Technical Specifications is adequate.
O j
Because the current Technical Specification provision authorized higher rates of pressurizer heatup than the correct limit, the question arose l
as to whether the correct limit of 100*F per hour has been exceeded in i
the past.
Discussions with Westinghouse indicate that this is unlikely.
This is because system capabilities and Technical Specification limits on the rate of reactor coolant system heatup and pressurization effec-i l
tively preclude pressurizer heatup rates in excess of 50*F to 75'F per hour.
Furthemore, the licensee reviewed the pressurizer and heater designs for Turkey Point after being informed of this potential i
problem and found that they are sized for a 55'F per hour heatup rate
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and therefore concluded that the heatup rate never exceeded 100*F per hour.
Accordingly, we concluce that the only action required by the i
licensee is mooification of the Technical Specifications to reduce the l
limiting pressurizer heatup rate of 200*F per hour to 100*F per hour.
O it is our understandins that Westin9nouse is perfomins a review of the stress analyses for canpanents of the reactor coolant pressure l
boundary to assure that no similar inadvertent error appears in any other pSrtion of the applicable Technical Specifications.
This action will be confimed by Westinghouse.
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l Environmental Consideration We have determined that the amendments do not authorize a change in i
effluent types or total amounts nor an increase in power level and will not result in any significant environmental impact.
Having made this i
detemination, we concluded that the amendments involve an action which
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is insignificant from the standpoint of environmental impact and pursuant l
i
i to 10 CFR 551.5(d) (4) that an environmental impact statement, or negative declaration and environmental impact appraisal need not be prepared in connection with the issuance of these amendments.
Conclusion l
We have concluded, based on the considerations discussed above, that:
(1) because the amendments do not involve a significant increase in the probability or consequences of accidents previously considered and do not involve a,significant decrease in a safety margin, the amendments do not involve a significant hazards consideration, (2) there is reasonable
({'S assurance that the health and safety of the public will not be endangered by operation in the proposed manner, and (3) such activities will be conducted in compliance with the Commission's regulations and issuance 7
of the amendments will not be inimical to the common defense and security l
or to the health and safety of the public.
Date:
October 25, 1978 l
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