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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046C3131993-07-28028 July 1993 LER 93-015-00:on 930630,HPCI Sys Declared Inoperable Due to Indicated Flow During Surveillance.Caused by Foreign Matl That Plugged Portion of Restricting Orifice.Restricting Orifice Removed,Cleaned & reinstalled.W/930728 Ltr ML20046B5241993-07-26026 July 1993 LER 93-007-01:on 930317,automatic Closing of RCIC Sys Turbine Steam Supply Isolation Valves Occurred Due to High Steam Flow Signal.Increased Frequency of Valve Testing from Monthly to weekly.W/930726 Ltr ML20045F8601993-06-30030 June 1993 LER 93-014-00:on 930531,automatic Scram Occurred,Resulting from Operation of Auxiliary Transformer Differential Relay During Power Ascension.Uat Phase B & C Differential Relays Left Interchanged as Investigative aid.W/930630 Ltr ML20045E2301993-06-25025 June 1993 LER 93-013-00:on 930530,RCIC Sys Declared Inoperable & 7 Day TS 3.5.D.2 LCO Entered Due to Speed Oscillations Which Occurred After Several Minutes of steady-state Operation. Caused by Actuator Failure.Actuator replaced.W/930625 Ltr ML20045E2251993-06-25025 June 1993 LER 93-012-00:on 930529,unplanned PCIS Group I Isolation Signal Occurred While Opening MSIV During Startup,Resulting in Automatic Closing of Related Valves.Caused by Licensed Operator Error.Group 1 Isolation reset.W/930625 Ltr ML20045D6941993-06-23023 June 1993 LER 93-011-00:on 930525,determined That Initial as-found Popping Pressures of Pilot Valves for Three Target Rock Main Steam Relief Valves Out of TS Tolerance.Caused by Setpoint Drift.Valves Reworked & Reassembled by Target Rock Corp ML20045D1861993-06-18018 June 1993 LER 93-010-00:on 930519,SUT Became de-energized During Planned Calibr of Turbine/Generator Relays Lockout Test While Shut Down.Caused by Personnel Error.Discussion Conducted W/Personnel Re Attention to detail.W/930618 Ltr ML20044H0441993-06-0202 June 1993 LER 93-009-00:on 930504,circuit Breaker Did Not Close During Planned Bus Transfer Due to Loose Control Circuit Wire.Lug Replaced & Reterminated on 930505 & Post Work Testing Completed W/Satisfactory results.W/930602 Ltr ML20024G7451991-04-24024 April 1991 LER 91-005-00:on 910325,diesel Generator Inoperable,Causing Loss of Ac Power to Train B Components of Safety Sys & Actuating Portions of Primary/Secondary Containment Sys. Caused by Voltage Regulator failure.W/910424 Ltr ML20029A6721991-02-25025 February 1991 LER 91-001-00:on 910125,automatic Primary Containment Isolation Control Sys Group 5 Actuation Occurred,Resulting in Closing of RCIC Turbine Steam Supply Isolation Valves. Caused by High Flow conditions.W/910225 Ltr ML20028G9731990-09-20020 September 1990 LER 89-036-01:on 891122,determined That HPCI Sys Inoperable Due to Inoperable Gland Seal Condenser Blower Motor.Caused by age-related Wear of Motor.Blower Motor Replaced & Blower Tested W/Satisfactory results.W/900920 Ltr ML20028G9121990-09-18018 September 1990 LER 89-037-01:on 891130,primary Containment/Traversing in-core Probe Ball Valve Discovered to Be Almost Full Open. Caused by Damage to Valve Stem Due to Manual Manipulation of Stem.Ball Valve & Solenoid Actuator replaced.W/900918 Ltr ML20043G3541990-06-12012 June 1990 LER 90-008-00:on 900513,automatic Scram Resulting from Load Rejection Occurred While at Full Power,Resulting in Trip of Generator Field Breakers.Caused by Fault on Offsite 345 Kv Transmission sys.Loss-of-field Relay replaced.W/900612 Ltr ML20043F8291990-06-0606 June 1990 LER 90-007-00:on 900507,discovered That Drywell to Suppression Chamber Vacuum Breaker Surveillance Not Performed Prior to Startup in 1988.Caused by Misunderstanding of requirements.W/900606 Ltr ML20042F5911990-04-30030 April 1990 LER 90-006-00:on 900330,determined That Position of Primary Containment Sys Isolation Valve Not Recorded Daily,Per Tech Specs.Review Performed to Determine If Other Problems Existed.Plant Shut Down & Review performed.W/900430 Ltr ML20012F5751990-04-0606 April 1990 LER 90-003-00:on 900311,automatic Actuation of Main Steam Sys Group 1 Portion of Primary Containment Isolation Control Sys Occurred.Caused by False High Reactor Vessel Water Level Signal.Procedure Developed Re backfill.W/900406 Ltr ML20012E9831990-03-30030 March 1990 LER 90-002-00:on 900228,determined That Max Fraction of Limiting Power Density Not Checked Daily During Reactor Power Operation,Per Tech Spec 4.1.B.On 900323,addl Tech Spec Issue Discovered.Tech Specs changed.W/900330 Ltr ML20012C4871990-03-12012 March 1990 LER 90-001-00:on 900209,24 H Limiting Condition for Operation Entered When Two RCS Instrumentation Excess Flow Check Valves Inappropriately Verified Operable During Testing.Cause Undetermined.Two Valves replaced.W/900312 Ltr ML20005G0981990-01-0808 January 1990 LER 89-038-00:on 891208,unplanned Automatic Reactor Protection Sys Scram Signal & Reactor Scram Occurred.Caused by False Low Reactor Vessel Water Level Signal.Local Level Indicators Satisfactorily calibr.W/900108 Ltr ML20005F8481990-01-0808 January 1990 LER 89-039-00:on 891209,automatic Actuation of RHR Sys Portion of Primary Containment Isolation Control Sys Occurred.Caused by Hydrodynamic Transient That Actuated Protective High Pressure switches.W/900108 Ltr ML20005E8551989-12-30030 December 1989 LER 89-037-00:on 891130,discovered That Traversing in-core Probe Ball Valve,Mfg by Consolidated Controls,Inc,Closed,In Violation of Tech Specs.Caused by Damage to Valve Stem.Ball Valve & Actuator replaced.W/891230 Ltr ML20011D1361989-12-11011 December 1989 LER 89-035-00:on 891111,inadvertent Actuation of Portion of Secondary Containment Sys During Surveillance Testing Occurred.Caused by Location of Radiation Isolation Control Sys Channel a Logic Relay.Procedure revised.W/891211 Ltr ML20005D7421989-12-0606 December 1989 LER 89-033-00:on 891106,automatic Actuation of Group 1 Portion of Primary Containment Isolation Control Sys (PCIS) Occurred.Caused by High Reactor Vessel Water Level.Manual Valve Closed & PCIS Logic Circuitry reset.W/891206 Ltr ML19351A4581989-12-0606 December 1989 LER 89-034-00:on 891108,determined That Reactor Pressure Exceeded 150 Psig on 891107 W/O Performing Surveillance Procedure 8.5.4.4, HPCI Valve Operability Test. Caused by Personnel Error.Procedure initiated.W/891206 Ltr ML19332D1421989-11-22022 November 1989 LER 89-031-00:on 891024,closing Times for Two in-series Primary Containment Isolation Valves Exceeded Acceptance Criteria During Shutdown Testing.Cause Undetermined.Closing Time Retested W/Satisfactory results.W/891122 Ltr ML19332D6231989-11-20020 November 1989 LER 89-032-00:on 891020,pneumatic Pressure Drop for Two of Four Automatic Depressurization Sys Accumulators Discovered Greater than Max Acceptable Value.Caused by Leakage from Seat of Supply Check Valves.Seat replaced.W/891120 Ltr ML19324C3181989-11-0909 November 1989 LER 88-002-01:on 880117,full Reactor Protection Sys Scram Trip Signal Occurred During Surveillance Test,Resulting in Incomplete Actuations.Caused by Procedure Inadequacy.Logic Relay Replaced & Procedure revised.W/891109 Ltr ML19324B1131989-10-21021 October 1989 LER 89-030-00:on 890926,control Room High Efficiency Air Filtration Sys Flowrate non-conservative Due to Procedure Error.Caused by Transcription Error.Procedure Revised & Test Reperformed Using Corrected procedure.W/891021 Ltr ML19325D4681989-10-16016 October 1989 LER 89-029-00:on 890914,locked High Radiation Area Door Found to Have Been Unsecured Contrary to Tech Spec 6.13.2. Caused by Failure to Adhere to Approved Procedures. Training on Access Requirements initiated.W/891016 Ltr ML19325D1861989-10-10010 October 1989 LER 89-028-00:on 890907,HPCI Sys Declared Inoperable Because Mechanical Overspeed Trip Occurred During Surveillance Test. Caused by Failure of Ramp Generator Signal Converter Module. Module Removed & Sent to Mfg for exam.W/891010 Ltr ML17277B8221984-07-20020 July 1984 LER 82-049/01X-1:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting.Caused by Personnel Error.Valve Removed & Replaced W/Properly Set Spare Valve. Procedure revised.W/840720 Ltr ML20024C3231983-06-24024 June 1983 Updated LER 82-038/03X-1:on 820817,RCIC Steam Line High Differential Pressure Alarm Received.Caused by Air in Sensing Lines to Pressure Switches.Cross Threaded Cap Found on in-line Snubber.Snubber replaced.W/830624 Ltr ML20024C2211983-06-24024 June 1983 Updated LER 80-053/03X-1:on 800814,0907 & 14,HPCI Turbine Exhaust Line Snubber 23-3-36 Determined Inoperable.Caused by Transient Hydrodynamic Shock During Startup & Shutdown. Snubbers upgraded.W/830624 Ltr ML20024B8451983-06-24024 June 1983 LER 83-031/03L-0:on 830528,HPCI Sys Made Inoperable to Repair Steam Leak on AO 2301-31.Caused by Leaking Stem Packing.Packing Replaced.Valve Tested Satisfactorily.Sys Returned to svc.W/830624 Ltr ML20024B8321983-06-24024 June 1983 LER 83-030/03L-0:on 830527,both HPCI Area Smoke Detection Sys Alarmed in Main Control Room.Caused by Valve A02301-31 Steam Leak Causing False Indications.Valve repaired.W/830624 Ltr ML20024C3101983-06-21021 June 1983 Updated LER 79-007/03X-1:on 790212,while Performing Test 8.7.4.3,valves AO-5033A,CV-5065-10,15,16 & 17 Failed to Give Proper Position Indication When Cycled & to Close within Specified Tolerance.Cause Not stated.W/830621 Ltr ML20024A8861983-06-16016 June 1983 LER 83-027/03L-0:on 830518,during Routine Insp,Folding Fire Door Found Inoperable.Caused by Operating Cable Becoming Detached from Pulley Due to Slack.Cable Reattached & Operating Mechanism adjusted.W/830616 Ltr ML20023D1691983-05-0909 May 1983 Updated LER 82-008/01X-1:on 820331,HPCI Injection Valve MO-2301-8 Failed to Open in Required Manner.Caused by Missing Wire Jumper Intended to Bypass Motor Operator Torque Switch.Jumper Installed & Valve Tested Satisfactorily ML20023D0671983-05-0909 May 1983 LER 83-021/03L-0:on 830411,during Surveillance Test 8.7.4.3, Primary Containment Isolation Valve AO-5033B Failed to Meet 10-s Closing Time Requirements.Caused by Lubricant Infiltrating Solenoid Valve Components.Components Replaced ML20023D0181983-05-0404 May 1983 LER 83-022/03L-0:on 830413,overload on Valve Motor 1301-17 Resulted in Loss of High Pressure Core Cooling Backup Capability.Caused by Oxidation in Motor End Bell & Motor Brushes,Due to Humidity Caused by Leaking Valve Packing ML20028G1591983-01-28028 January 1983 LER 83-002/01T-0:on 830116,flow Ref off-normal Alarm Received.Average Power Range Monitor Flux Scram Trip Settings Affected.Cause Under Investigation.Flow Inputs Monitored & Amplifier B Recalibr ML20028F4121983-01-17017 January 1983 LER 83-002/01X-0:on 830116,while Clearing off-normal Alarm for Flow Comparators,Average Power Range Monitor Flux Scram Trip Settings Found in Nonconservative Direction.Caused by Drifting Proportional Amplifiers.Settings Checked Daily ML20028B0421982-11-16016 November 1982 LER 82-049/01T-0:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting of 1240 Psig, Exceeding Tech Specs.Caused by Personnel Error.Set Valve Removed,Procedure Adherence Stressed & Procedure Revised ML20027C9801982-10-20020 October 1982 LER 82-039/03L-0:on 820920,timing Tests of Three Reactor Water Cleanup Isolation Valves 1201-2,-5 & -80 Not Completed within Allowed Time.Caused by Operational Constraints Requiring Testing at Reduced Power ML20027C9941982-10-20020 October 1982 LER 82-040/03L-0:on 820920,found Reactor Protection Sys Initiation Function of Turbine Stop Valve Completed 1 Day Late.Caused by Decision to Defer Test Due to MSIV D Line Isolation.Tracking Sys Implemented to Prevent Recurrences ML20052B9141982-04-23023 April 1982 LER 82-010/03L-0:on 820326,during Review of Testing Requirements,Surveillance Test 8.I.4 Standby Liquid Control Sys Found Not Verified.Caused by Breakdown in Multidiscipline Review of Results ML20052F2071982-04-14014 April 1982 Updated LER 81-060/03X-1:on 811020,determined Potential Exists to Reduce Number of Operable APRM & IRM Instrument Channels in Rod Block Trip Sys to Below Tech Spec Min ML20050A6321982-03-19019 March 1982 Updated LER 82-055/01T-1:on 810926,during Shutdown,Yarway Level Indicators Started Oscillating.Drywell Temp Was 240 F at 81-ft W/Elevation Coolant Temp 220 F.Caused by Ineffective Drywell Cooling.Ventilation Returned to Svc ML20050A4521982-03-19019 March 1982 LER 82-006/01T-0:on 820304,while Performing Maint Re SIL 352 on Pressure Adjustment Mechanism HPCI Stop Valve,Three Broken cap-screws Found.No Cause Determined.Screws Examined, Replaced & Sys Returned to Svc ML20050A4331982-03-19019 March 1982 Updated LER 81-062/01X-1:on 811116,Wyle Labs Informed Util That Two Target Rock Safety Relief Valves Had Not Passed Setpoint Tests.Caused by Setpoint Shift Due to Changes to Designed Differential Forces from Excessive Pilot Leakage 1993-07-28
[Table view] Category:RO)
MONTHYEARML20046C3131993-07-28028 July 1993 LER 93-015-00:on 930630,HPCI Sys Declared Inoperable Due to Indicated Flow During Surveillance.Caused by Foreign Matl That Plugged Portion of Restricting Orifice.Restricting Orifice Removed,Cleaned & reinstalled.W/930728 Ltr ML20046B5241993-07-26026 July 1993 LER 93-007-01:on 930317,automatic Closing of RCIC Sys Turbine Steam Supply Isolation Valves Occurred Due to High Steam Flow Signal.Increased Frequency of Valve Testing from Monthly to weekly.W/930726 Ltr ML20045F8601993-06-30030 June 1993 LER 93-014-00:on 930531,automatic Scram Occurred,Resulting from Operation of Auxiliary Transformer Differential Relay During Power Ascension.Uat Phase B & C Differential Relays Left Interchanged as Investigative aid.W/930630 Ltr ML20045E2301993-06-25025 June 1993 LER 93-013-00:on 930530,RCIC Sys Declared Inoperable & 7 Day TS 3.5.D.2 LCO Entered Due to Speed Oscillations Which Occurred After Several Minutes of steady-state Operation. Caused by Actuator Failure.Actuator replaced.W/930625 Ltr ML20045E2251993-06-25025 June 1993 LER 93-012-00:on 930529,unplanned PCIS Group I Isolation Signal Occurred While Opening MSIV During Startup,Resulting in Automatic Closing of Related Valves.Caused by Licensed Operator Error.Group 1 Isolation reset.W/930625 Ltr ML20045D6941993-06-23023 June 1993 LER 93-011-00:on 930525,determined That Initial as-found Popping Pressures of Pilot Valves for Three Target Rock Main Steam Relief Valves Out of TS Tolerance.Caused by Setpoint Drift.Valves Reworked & Reassembled by Target Rock Corp ML20045D1861993-06-18018 June 1993 LER 93-010-00:on 930519,SUT Became de-energized During Planned Calibr of Turbine/Generator Relays Lockout Test While Shut Down.Caused by Personnel Error.Discussion Conducted W/Personnel Re Attention to detail.W/930618 Ltr ML20044H0441993-06-0202 June 1993 LER 93-009-00:on 930504,circuit Breaker Did Not Close During Planned Bus Transfer Due to Loose Control Circuit Wire.Lug Replaced & Reterminated on 930505 & Post Work Testing Completed W/Satisfactory results.W/930602 Ltr ML20024G7451991-04-24024 April 1991 LER 91-005-00:on 910325,diesel Generator Inoperable,Causing Loss of Ac Power to Train B Components of Safety Sys & Actuating Portions of Primary/Secondary Containment Sys. Caused by Voltage Regulator failure.W/910424 Ltr ML20029A6721991-02-25025 February 1991 LER 91-001-00:on 910125,automatic Primary Containment Isolation Control Sys Group 5 Actuation Occurred,Resulting in Closing of RCIC Turbine Steam Supply Isolation Valves. Caused by High Flow conditions.W/910225 Ltr ML20028G9731990-09-20020 September 1990 LER 89-036-01:on 891122,determined That HPCI Sys Inoperable Due to Inoperable Gland Seal Condenser Blower Motor.Caused by age-related Wear of Motor.Blower Motor Replaced & Blower Tested W/Satisfactory results.W/900920 Ltr ML20028G9121990-09-18018 September 1990 LER 89-037-01:on 891130,primary Containment/Traversing in-core Probe Ball Valve Discovered to Be Almost Full Open. Caused by Damage to Valve Stem Due to Manual Manipulation of Stem.Ball Valve & Solenoid Actuator replaced.W/900918 Ltr ML20043G3541990-06-12012 June 1990 LER 90-008-00:on 900513,automatic Scram Resulting from Load Rejection Occurred While at Full Power,Resulting in Trip of Generator Field Breakers.Caused by Fault on Offsite 345 Kv Transmission sys.Loss-of-field Relay replaced.W/900612 Ltr ML20043F8291990-06-0606 June 1990 LER 90-007-00:on 900507,discovered That Drywell to Suppression Chamber Vacuum Breaker Surveillance Not Performed Prior to Startup in 1988.Caused by Misunderstanding of requirements.W/900606 Ltr ML20042F5911990-04-30030 April 1990 LER 90-006-00:on 900330,determined That Position of Primary Containment Sys Isolation Valve Not Recorded Daily,Per Tech Specs.Review Performed to Determine If Other Problems Existed.Plant Shut Down & Review performed.W/900430 Ltr ML20012F5751990-04-0606 April 1990 LER 90-003-00:on 900311,automatic Actuation of Main Steam Sys Group 1 Portion of Primary Containment Isolation Control Sys Occurred.Caused by False High Reactor Vessel Water Level Signal.Procedure Developed Re backfill.W/900406 Ltr ML20012E9831990-03-30030 March 1990 LER 90-002-00:on 900228,determined That Max Fraction of Limiting Power Density Not Checked Daily During Reactor Power Operation,Per Tech Spec 4.1.B.On 900323,addl Tech Spec Issue Discovered.Tech Specs changed.W/900330 Ltr ML20012C4871990-03-12012 March 1990 LER 90-001-00:on 900209,24 H Limiting Condition for Operation Entered When Two RCS Instrumentation Excess Flow Check Valves Inappropriately Verified Operable During Testing.Cause Undetermined.Two Valves replaced.W/900312 Ltr ML20005G0981990-01-0808 January 1990 LER 89-038-00:on 891208,unplanned Automatic Reactor Protection Sys Scram Signal & Reactor Scram Occurred.Caused by False Low Reactor Vessel Water Level Signal.Local Level Indicators Satisfactorily calibr.W/900108 Ltr ML20005F8481990-01-0808 January 1990 LER 89-039-00:on 891209,automatic Actuation of RHR Sys Portion of Primary Containment Isolation Control Sys Occurred.Caused by Hydrodynamic Transient That Actuated Protective High Pressure switches.W/900108 Ltr ML20005E8551989-12-30030 December 1989 LER 89-037-00:on 891130,discovered That Traversing in-core Probe Ball Valve,Mfg by Consolidated Controls,Inc,Closed,In Violation of Tech Specs.Caused by Damage to Valve Stem.Ball Valve & Actuator replaced.W/891230 Ltr ML20011D1361989-12-11011 December 1989 LER 89-035-00:on 891111,inadvertent Actuation of Portion of Secondary Containment Sys During Surveillance Testing Occurred.Caused by Location of Radiation Isolation Control Sys Channel a Logic Relay.Procedure revised.W/891211 Ltr ML20005D7421989-12-0606 December 1989 LER 89-033-00:on 891106,automatic Actuation of Group 1 Portion of Primary Containment Isolation Control Sys (PCIS) Occurred.Caused by High Reactor Vessel Water Level.Manual Valve Closed & PCIS Logic Circuitry reset.W/891206 Ltr ML19351A4581989-12-0606 December 1989 LER 89-034-00:on 891108,determined That Reactor Pressure Exceeded 150 Psig on 891107 W/O Performing Surveillance Procedure 8.5.4.4, HPCI Valve Operability Test. Caused by Personnel Error.Procedure initiated.W/891206 Ltr ML19332D1421989-11-22022 November 1989 LER 89-031-00:on 891024,closing Times for Two in-series Primary Containment Isolation Valves Exceeded Acceptance Criteria During Shutdown Testing.Cause Undetermined.Closing Time Retested W/Satisfactory results.W/891122 Ltr ML19332D6231989-11-20020 November 1989 LER 89-032-00:on 891020,pneumatic Pressure Drop for Two of Four Automatic Depressurization Sys Accumulators Discovered Greater than Max Acceptable Value.Caused by Leakage from Seat of Supply Check Valves.Seat replaced.W/891120 Ltr ML19324C3181989-11-0909 November 1989 LER 88-002-01:on 880117,full Reactor Protection Sys Scram Trip Signal Occurred During Surveillance Test,Resulting in Incomplete Actuations.Caused by Procedure Inadequacy.Logic Relay Replaced & Procedure revised.W/891109 Ltr ML19324B1131989-10-21021 October 1989 LER 89-030-00:on 890926,control Room High Efficiency Air Filtration Sys Flowrate non-conservative Due to Procedure Error.Caused by Transcription Error.Procedure Revised & Test Reperformed Using Corrected procedure.W/891021 Ltr ML19325D4681989-10-16016 October 1989 LER 89-029-00:on 890914,locked High Radiation Area Door Found to Have Been Unsecured Contrary to Tech Spec 6.13.2. Caused by Failure to Adhere to Approved Procedures. Training on Access Requirements initiated.W/891016 Ltr ML19325D1861989-10-10010 October 1989 LER 89-028-00:on 890907,HPCI Sys Declared Inoperable Because Mechanical Overspeed Trip Occurred During Surveillance Test. Caused by Failure of Ramp Generator Signal Converter Module. Module Removed & Sent to Mfg for exam.W/891010 Ltr ML17277B8221984-07-20020 July 1984 LER 82-049/01X-1:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting.Caused by Personnel Error.Valve Removed & Replaced W/Properly Set Spare Valve. Procedure revised.W/840720 Ltr ML20024C3231983-06-24024 June 1983 Updated LER 82-038/03X-1:on 820817,RCIC Steam Line High Differential Pressure Alarm Received.Caused by Air in Sensing Lines to Pressure Switches.Cross Threaded Cap Found on in-line Snubber.Snubber replaced.W/830624 Ltr ML20024C2211983-06-24024 June 1983 Updated LER 80-053/03X-1:on 800814,0907 & 14,HPCI Turbine Exhaust Line Snubber 23-3-36 Determined Inoperable.Caused by Transient Hydrodynamic Shock During Startup & Shutdown. Snubbers upgraded.W/830624 Ltr ML20024B8451983-06-24024 June 1983 LER 83-031/03L-0:on 830528,HPCI Sys Made Inoperable to Repair Steam Leak on AO 2301-31.Caused by Leaking Stem Packing.Packing Replaced.Valve Tested Satisfactorily.Sys Returned to svc.W/830624 Ltr ML20024B8321983-06-24024 June 1983 LER 83-030/03L-0:on 830527,both HPCI Area Smoke Detection Sys Alarmed in Main Control Room.Caused by Valve A02301-31 Steam Leak Causing False Indications.Valve repaired.W/830624 Ltr ML20024C3101983-06-21021 June 1983 Updated LER 79-007/03X-1:on 790212,while Performing Test 8.7.4.3,valves AO-5033A,CV-5065-10,15,16 & 17 Failed to Give Proper Position Indication When Cycled & to Close within Specified Tolerance.Cause Not stated.W/830621 Ltr ML20024A8861983-06-16016 June 1983 LER 83-027/03L-0:on 830518,during Routine Insp,Folding Fire Door Found Inoperable.Caused by Operating Cable Becoming Detached from Pulley Due to Slack.Cable Reattached & Operating Mechanism adjusted.W/830616 Ltr ML20023D1691983-05-0909 May 1983 Updated LER 82-008/01X-1:on 820331,HPCI Injection Valve MO-2301-8 Failed to Open in Required Manner.Caused by Missing Wire Jumper Intended to Bypass Motor Operator Torque Switch.Jumper Installed & Valve Tested Satisfactorily ML20023D0671983-05-0909 May 1983 LER 83-021/03L-0:on 830411,during Surveillance Test 8.7.4.3, Primary Containment Isolation Valve AO-5033B Failed to Meet 10-s Closing Time Requirements.Caused by Lubricant Infiltrating Solenoid Valve Components.Components Replaced ML20023D0181983-05-0404 May 1983 LER 83-022/03L-0:on 830413,overload on Valve Motor 1301-17 Resulted in Loss of High Pressure Core Cooling Backup Capability.Caused by Oxidation in Motor End Bell & Motor Brushes,Due to Humidity Caused by Leaking Valve Packing ML20028G1591983-01-28028 January 1983 LER 83-002/01T-0:on 830116,flow Ref off-normal Alarm Received.Average Power Range Monitor Flux Scram Trip Settings Affected.Cause Under Investigation.Flow Inputs Monitored & Amplifier B Recalibr ML20028F4121983-01-17017 January 1983 LER 83-002/01X-0:on 830116,while Clearing off-normal Alarm for Flow Comparators,Average Power Range Monitor Flux Scram Trip Settings Found in Nonconservative Direction.Caused by Drifting Proportional Amplifiers.Settings Checked Daily ML20028B0421982-11-16016 November 1982 LER 82-049/01T-0:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting of 1240 Psig, Exceeding Tech Specs.Caused by Personnel Error.Set Valve Removed,Procedure Adherence Stressed & Procedure Revised ML20027C9801982-10-20020 October 1982 LER 82-039/03L-0:on 820920,timing Tests of Three Reactor Water Cleanup Isolation Valves 1201-2,-5 & -80 Not Completed within Allowed Time.Caused by Operational Constraints Requiring Testing at Reduced Power ML20027C9941982-10-20020 October 1982 LER 82-040/03L-0:on 820920,found Reactor Protection Sys Initiation Function of Turbine Stop Valve Completed 1 Day Late.Caused by Decision to Defer Test Due to MSIV D Line Isolation.Tracking Sys Implemented to Prevent Recurrences ML20052B9141982-04-23023 April 1982 LER 82-010/03L-0:on 820326,during Review of Testing Requirements,Surveillance Test 8.I.4 Standby Liquid Control Sys Found Not Verified.Caused by Breakdown in Multidiscipline Review of Results ML20052F2071982-04-14014 April 1982 Updated LER 81-060/03X-1:on 811020,determined Potential Exists to Reduce Number of Operable APRM & IRM Instrument Channels in Rod Block Trip Sys to Below Tech Spec Min ML20050A6321982-03-19019 March 1982 Updated LER 82-055/01T-1:on 810926,during Shutdown,Yarway Level Indicators Started Oscillating.Drywell Temp Was 240 F at 81-ft W/Elevation Coolant Temp 220 F.Caused by Ineffective Drywell Cooling.Ventilation Returned to Svc ML20050A4521982-03-19019 March 1982 LER 82-006/01T-0:on 820304,while Performing Maint Re SIL 352 on Pressure Adjustment Mechanism HPCI Stop Valve,Three Broken cap-screws Found.No Cause Determined.Screws Examined, Replaced & Sys Returned to Svc ML20050A4331982-03-19019 March 1982 Updated LER 81-062/01X-1:on 811116,Wyle Labs Informed Util That Two Target Rock Safety Relief Valves Had Not Passed Setpoint Tests.Caused by Setpoint Shift Due to Changes to Designed Differential Forces from Excessive Pilot Leakage 1993-07-28
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217E3021999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Pilgrim Nuclear Station.With ML20212C2921999-09-16016 September 1999 SER Accepting Licensee Request for Relief from ASME Code Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Pilgrim Nuclear Power Station ML20216F3511999-09-0808 September 1999 ISI Summary Rept for Refuel Outage 12 at Pnps ML20216E6881999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pilgrim Nuclear Power Station.With ML20210R3401999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Pilgrim Nuclear Power Station.With ML20209C4731999-07-0707 July 1999 Addendum to SE on Proposed Transfer of Operating License & Matls License from Boston Edison Co to Entergy Nuclear Generation Co ML20209H8251999-07-0101 July 1999 Provides Commission with Evaluation of & Recommendations for Improvement in Processes Used in Staff Review & Approval of Applications for Transfer of Operating Licenses of TMI-1 & Pilgrim Station ML20209E6191999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Pilgrim Nuclear Power Station.With ML20196H2451999-06-29029 June 1999 SER Denying Licensee Proposed Alternative in Relief Request PRR-13,rev 2.Staff Determined That Proposed Alternative Provides Insufficient Info to Determine Adequacy of Scope of Implementation ML20209A8901999-06-28028 June 1999 SER Accepting Licensee Proposed Alternative to Use Code Case N-573 for Remainder of 10-year Interval Pursuant to 10CFR50.55a(a)(3)(i) ML20209B9861999-06-23023 June 1999 Rev 13A to Pilgrim Nuclear Power Station COLR for Cycle 13 ML20217N9061999-06-21021 June 1999 Rept of Changes,Tests & Experiments for Period of 970422-990621 ML20195K3431999-06-15015 June 1999 Safety Evaluation Granting Licensee Request to Use Guidance of GL 90-05 to Repair Flaws in ASME Class 3 Salt Svc Water System Piping for Plant ML20195G8231999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Pnps.With ML20207E7471999-05-27027 May 1999 Safety Evaluation Granting Request Re Reduction of IGSCC Insp of Category D Welds Due to Implementation of HWC to License DPR-35 ML20206M1971999-05-11011 May 1999 SER Accepting Request for Approval to Repair Flaws in ASME Code Class 3 Salt Svc Water Piping at Plant ML20206J6611999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Pilgrim Nuclear Power Station.With ML20205L0221999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Pilgrim Nuclear Power Station.With ML20207J5471999-03-0909 March 1999 Training Simulator,1999 4-Yr Certification Rept ML20207F9401999-03-0101 March 1999 Long Term Program Semi-Annual Rept for Pilgrim Nuclear Power Station ML20207H5451999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Pilgrim Nuclear Power Station.With ML20196E2151998-12-31031 December 1998 1998 Annual Rept for Boston Edison & Securities & Exchange Commission Form 10-K Rept.With ML20206Q2741998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Pilgrim Nuclear Power Station.With ML20197J3591998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Pilgrim Nuclear Power Station.With ML20195C9951998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Pilgrim Nuclear Power Station.With ML20154K0721998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Pilgrim Nuclear Power Station.With ML20153D3901998-09-22022 September 1998 Safety Evaluation Granting 970707 Request to Use Guidance in GL 90-05 to Repair Flaws in ASME Class 3 Salt Svc Water Sys Piping for Pilgrim Nuclear Power Station ML20197C5011998-09-0404 September 1998 Rev 12C,Pages 4 & 5 to Pilgrim Nuclear Power Station Colr ML20197C5471998-08-31031 August 1998 Rev 12C to Pilgrim Nuclear Power Station Colr ML20151W8231998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Pilgrim Nuclear Power Station.With ML20237E2251998-08-26026 August 1998 Suppl & Revs to SE for Amend 173 for Pigrim Nuclear Power Station ML20237A9941998-07-31031 July 1998 Monthly Operating Rept for Pilgrim Nuclear Power Station ML20236U8201998-07-13013 July 1998 Rev 12B to Pilgrim Nuclear Power Station COLR (Cycle 12) ML20236P0151998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Pilgrim Nuclear Power Station ML20249A3741998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Pilgrim Nuclear Power Station.W/Undated Ltr ML20247H2081998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Pilgrim Nuclear Power Station ML20207B7601998-03-31031 March 1998 Final Rept, Pilgrim Nuclear Power Station Site-Specific Offsite Radiological Emergency Preparedenss Prompt Alert & Notification System Quality Assurance Verification, Prepared for FEMA ML20216G3911998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Pilgrim Nuclear Power Station ML20216J3741998-03-19019 March 1998 Safety Evaluation Accepting Licensee Request to Evaluate Elevated Tailpipe Temp on Safety Relief Valve SRV 203-3B ML20248L2241998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Pilgrim Nuclear Station ML20202G5251998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Pilgrim Nuclear Power Station ML20236M8511997-12-31031 December 1997 1997 Annual Rept for Boston Edison & Securities & Exchange Commission Form 10-K Rept ML20198L7701997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Pilgrim Nuclear Power Station ML20203D6101997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Pilgrim Nuclear Power Station ML20202D5761997-11-0808 November 1997 1997 Evaluated Exercise BECO-LTR-97-111, Monthly Operating Rept for Oct 1997 for Pilgrim Nuclear Power Station1997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Pilgrim Nuclear Power Station ML20217D6431997-10-0101 October 1997 Safety Evaluation Granting Request for Approval to Repair Flaws in Accordance W/Gl 90-05 for ASME Class 3 SSW Piping for Pilgrim ML20217H5621997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Pilgrim Nuclear Power Station ML20216J4131997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Pilgrim Nuclear Power Station ML20210J3321997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Pilgrim Nuclear Power Station 1999-09-08
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ff 10 CFR 50.73 BOSTON EDISON Pilgrim Nuclear Power Station Rocky Hdi Road Plymouth, Massachusetts o236o E. T. Boulette, PhD Senior Vice President-Nuclear June 25 , 1993 BECo Ltr. 93- 80 U.S. Nuclear Regulatory Commission Attn: -Document Control Desk Washington, D.C. 20555 Docket No. 50-293 License No. DPR-35 The enclosed Licensee Event Report (LER) 93-012-00, " Group 1 Isolation During Startup While Opening Main Steam Isolation Valve", is submitted in accordance with 10 CFR Part 50.73.
Please do not hesitate to contact me if there are any questions regarding this report.
'l bC E. T. Boulette, PhD WJM/bal
Enclosure:
LER 93-012-00 cc: Mr.- Thomas T. Martin Regional Administrator, Region I U.S. Nuclear Regulatory Commission 475 Allendale Rd.
King of Prussia, PA 19406 Mr. R. B. Eaton Div. of Reactor Projects I/II Office of NRR - USNRC One White Flint North - Mail Stop 14D1 11555 Rockville Pike Rockville, MD 20852 Sr. NRC Resident Inspector - Pilgrim Station
. Standard BEco LER Distribution 010032 9307010266 930625 /
PDR S
ADOCK 05000293 //, [)
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NRC FOnM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 (5+921 EXPIRES 5/31/95
, FSTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS LICENSEE EVENT REPORT (LER) 2"*O G M E R M ETWO L O C AND RECORDS MANAGEMENT BRAfCH (MNBH T714), U.S. NUCLEAR REGULATORY COMMIPSiON, WASHINGTON, DC 205550001, AND TO THE PAPERWORK REDUCTION PFnECT (31540104), OFTICE (See reverse for riumber of digite/charriers for each block) OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) l PAGE(3)
PILGRIM NUCLEAR POWER STATION 05000 - 293 g 1 of 5 YiTLE (4)
Group 1 Isolation During Startup While Opening Main Steam isolation Valve EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
SEQUENTIAL REVIS10N F ACluTY NAME DOCKET NUMBER MOMH DM YEAR YEAR NUMBER NUMBER MONTH DAY YEAR N/A 05000 FACIUTY NAME DOCKET NUMBER 05 29 93 93 012 00 06 25 93 N/A 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REOUIREMENTS OF 10 CFR S (Check one or more)(11)
IN 20.402(b) 20.405(c) X 50.73(a)(2)(iv) 73.71(b)
PO 20.405(a)(1)(i) 50.36(c)(1) 50.73(a)(2)(v)
LE E 001 73.71(c) 0)
20.405(a)(1)(ii) 50.36(c)(2) 50.73(a)(2)(vii) OTHER 20.405(a)(1)(iii) 50.73(a)(2)(i) 50.73(a)(2)(viii)(A) g7ggg (g ,c,,y 20.405(a)(1)(iv) 50.73(a)(2)(ii) 50.73(a)(2)(viii)(B) ytgige,cy 20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x) Form 366A)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER (include Area Code)
William J. Munro - Sr. Compliance Engineer (508) 747-8474 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFACTURER CAUSE SYSTEM COMPONENT MANUFACTURER SUPPLEMENTAL REPORT EXPECTED (14) *"'" D# "
EXPECTED YES NO SUBMISSION i e yes, compeie EXPECTED SUBMISSION DATE)
X DATE (15) j ABSTRACT On May 29, 1993 at 0614 hours0.00711 days <br />0.171 hours <br />0.00102 weeks <br />2.33627e-4 months <br />, an unplanned Primary Containment Isolation Control System ;
(PCIS) Group 1 isolation signal occurred while opening a Main Steam Isolation Valve (MSIV) during startup. The signal resulted in the automatic closing of the related_ valves. The isolation signal was caused by a high Reactor Vessel (RV) water level (+48 inches). The high water level occurred while opening an MSIV that caused a swell (expansion) of RV water. The root cause of the event was licensed operator error. While attempting to equalize steam line pressures, a misunderstood communication occurred between an operator and the Nuclear Watch Engineer regarding the RV water level and RV pressure. This caused the NWE to leave the 'C' inboard main steam isolation valve open longer than planned, resulting in a relatively greater decrease in RV pressure and a corresponding rise in RV water level to the point (+48 inches) where the high water level isolation occurred.
Contributing to the event was the fact that the MSIVs were opened with RV water level starting slightly higher than that directed by the applicable procedure and several manual isolation valves downstream of the MSIVs, thought to be closed, were open resulting in increased steam flow through the MSIV when opening the valve. The importance of procedural adherence and clear communication was stressed by the Chief Operating Engineer to the applicable Watch Engineer. Procedure 2.2.92 will be revised to ensure that applicable valves are checked in the event outboard steam pressure does not build up.
This event occurred during a startup with the reactor mode selector switch in the STARTUP position. The control rods were in a partially withdrawn position. The RV water temperature was 350 degrees Fahrenheit and the RV pressure was 140 psig. The reactor l power level was approximately one percent. This report is submitted in accordance with '
10 CFR 50.73(a)(2)(iv). This event posed no threat to the health and safety of the public.
NnC rORu a m i
NRC FORM 366A U.S. NUCLEAR HEGULATORY COMMISSION APPROVE BY O 8 0 3150-0104-LICENSEE EVENT REPORT (LER) fraL"Taa"iu"a L "J' %'a g gng g gEu g g o gnu TEXT CONTINUATION 8 em s ANo mGgt OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20501 FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) - PAGE (2)
EAR WBW "
R 20f 5 PILGRIM NUCLEAR POWER STATION 05000-293 93 - 012- 00 VEXT (if more space is required, use additional copies of NRC Form 366A)(17)
EVENT DESCRIPTION .
On May 29,1993 at 0614 hours0.00711 days <br />0.171 hours <br />0.00102 weeks <br />2.33627e-4 months <br />, an unplanned Primary Con'tainment Isolation Control System '
(PCIS) Group 1 (one) isolation signal occurred. The signal was the result of'a high water .
level-in the Reactor Vessel that occurred while opening Main Steam System isolation valve:
(MSIV) A0-203-10. The MSIV was being opened with a differential pressure of approximately 140 psid across the seat of the MSIV.
The signal resulted in the following responses:
- The outboard MSIVs A0-203-2A/B/C/D, in the open position, closed automatically.
- The inboard MSIVs A0-203-1A/B/0, in the closed position, remained. closed. .
- The inboard MSIV A0-203-10 closed automatically.
- The. inboard and outboard Main Steam drain line isolation valves M0-220-1 and M0-220-2, in the open position, closed automatically. 1
- The inboard and outboard Sample System Valves A0-220-44 and -45, in-the open position, closed automatically. 't After reducing the RV water level, the isolation signal was reset.
Problem Report 93.9279 was written to document the. event. The NRC Operations Center was notified in accordance with 10 CFR 50.72 at 0810 hour0.00938 days <br />0.225 hours <br />0.00134 weeks <br />3.08205e-4 months <br />s:on May 29, 1993.
This event occurred during a startup with the reactor. mode selector switch in the STARTUP position. The control rods were in a partially withdrawn position. The Reactor' Vessel- '
(RV) water temperature was 350 degrees Fahrenheit and the RV pressure was 140 psig. The.-
reactor power . level was approximately one percent. The RV water level was being ~ manually ; J controlled and was approximately-+26 inches just prior to'the event.
CAUSE The cause for the high RV water level trip signal was the swell (expansion); of.the RV.
water that. occurred when the "C" inboard MSIV A0-203-1C.was opened with the."C" outboard-MSIV A0-203-2C in the open position. The root'cause was utility licensed operator error. 1 Following refueling outage No. 9.the plant was stsrted up with MSIVs closed to perform pre-op testing on the main turbine. .On May 29, 1993 operations personnel were performing-activities to restart the plant using Procedure 2.1.3,(Rev. 23) "Startup With MSIVs closed ,
Rx Pre'sures Less Than 600 psig." The Nuclear Watch Engineer (NWE) had indicated.that the-inboard MSIVs would have to be opened prior to pressurizing the reactor greater ~than 150 psig. ;
NRC FCFW 366A @e2)
. - 1 RRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSloN APPROVED BY OMB NO,3150-0104 r s-m EXPIRES 5/31/95
. ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS LICENSEE EVENT REPORT (LER) 1""Of"REaTseTnc"eWEJfoE,4R%"*Ts TEXT CONTINUATION Su"[' DRYSIs'SEwYw"8c"ufE$Mo"oN"
$usEEEE7AND UDO AS T N, FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (2)
YEAR R MB 30f 5 PILGRIM NUCLEAR POWER STATION 05000-293 93 - -012- 00 TEXT (if more space is required, use additional copies of NRC Form 366A)(17)
The operators were using Procedure 2.2.92 (Rev. 25) " Main Steam Isolation and Turbine Bypass Valves". Section 7.1 " Opening MSIVs with Reactor Pressurized" instructs the operators to open the outboard MSIVs, equalize the main steam header and reactor pressures within 50 psig and then open the inboard MSIVs one at a time. Procedure 2.2.92 also contains a CAUTION statement to maintain a lower initial RV water level in the low end of the normal operating range at less than 24" to account for " swell" during opening of the MSIVs.
The valve lineup was configured to drain condensed steam from the main steam lines.
Following a warm-up of the drain lines, drain valve M0-220-04 was closed in an attempt to pressurize the main steam lines and obtain a 50 psi differential across the MSIVs (50 psid is the preferred differential; a maximum of 200 psid is allowed). After an hour there was no increase in pressure.
After discussion with the Chief Operating Engineer a decision was made by the NWE to open the inboard MSIVs for short periods of time to pressurize the lines. The reactor pressure was 140 psig. Control room operators were assigned to monitor reactor water level and outboard steam pressure, and to announce the parameters as each MSIV was opened.
Following the individual opening of the "A" and "B" inboard MSIVs the reactor water level swelled from +28 inches to +43 inches and +28 inches to +39 inches for "A" and "B" MSIVs respectively. The pressure in the outboard steam lines increased only slightly. When the NWE opened the "C" inboard MSIV a misunderstood communication occurred. The NWE misunderstood the announced steam line pressure as the RV water level and did not close the "C" inboard MSIV. RV water swelled from approximately +26 inches to approximately +48 inches and thereby resulted in the event.
CONTRIBUTING CAUSE Failure to follow Procedure 2.2.92 by lowering the reactor water level to 26" vice 24" to account for " swell" during opening of the MSIVs.
When the next shift crew performed a review of the main steam lineup, the steam supply valve-(H0-170) to the electrolytic compression modules and the SJAE Regulator Bypass valve (H0-160) were found in the open position. In addition, the "A" primary jet steam supply valve was frozen in the open position. Failure to isolate these valves prevented steam pressure from building up in the outboard steam lines.
CORRECTIVE ACTION On May 29, 1993 the Group 1 isolation was reset per Procedure 2.2.125.1 Reset Of Primary And Secondary Isolations, water level was restored and downstream steam auxiliary valves were closed allowing downstream piping to pressurize.
Procedure 2.2.92 will be revised to ensure that applicable valves are checked in the event outboard steam pressure does not build up, we um umm
, - . . . - . , - - . . . _ .~ . ~ ~ - - . . .. - .
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVEo BY OM8 NO.3150-0104 mm EXPlRES 5/31/95 ;
ESTlMATED BURDEN PER RESPONSE 'O COMPLV WITH THIS Di LICENSEE EVENT REPORT (LER) 1"3?%2fLsfEisjA O INF T TEXT CONTINUATION 35To"m cSou SS"8EsHS"oTTEANaNm -
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A FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (2) ,
vem Wa?c EE 4of 5 PILGRIM NUCLEAR POWER STATION 05000-293 g3 . - -012- 00-TEXT (if more space is required, use additional copies of NHC Form 366A)(17)
A discussion was held between the Operations Section Manager, the Chief Operating Engineer '
and the applicable Nuclear Watch Engineer to stress the importance of procedural adherence and clear communications.
This event will be reviewed with all operating crews during Licensed Operator j Requalification. training. -
SAFETY CONSE0VENCES This event posed no threat to the health and safety of the public. ;
The purpose of the RV high water level isolation is to protect against rapid .
i depressurization due to malfunction of the pressure regulator system during.startup when y; RV pressure is below 880 psig. ~!
The high RV water level trip signal resulted from the swell .(expansion).of RV water that occurred when the Main Steam line 'C' outboard MSIV was opened. The closing of.the Group 1 (one) isolation valves was the designed response to the high RV water level.
This report is submitted in accordance with 10 CFR 50.73(a)(2)(iv) because the closing of isolation valves, although a designed response, was not planned.
SIMILARITY TO PREVIOUS EVENTS A review was conducted of Pilgrim Station Licensee Event Reports (LERs) submitted since-January 1984. The review was focused to LERs submitted in accordance with- .
i 10 CFR 50.73(a)(2)(iv) that involved a similar event resulting from a high RV water level. :
The review identified events reported-in LERs 50-293/89-007-00 and 92-004-00.
For LER 92-004-00, three Group 1 isolations occurred during a shutdown on-March 26-27, 1992. The second isolation occurred on March 26, 1992, at 2129 hours0.0246 days <br />0.591 hours <br />0.00352 weeks <br />8.100845e-4 months <br />, after the PCIS Group I circuitry was reset and while opening the-MSIVs with the RV pressure at q 82 psig and RV water level at +29 inches. The cause was high RV water level due'~ to swell; '
Prior to opening MSIV A0-203-10, the Main Steam header pressure:and RV pressure was:
equalized within. 50 psig in accordance with procedure 2.2.92 (Rev. 24)- section-7.1.-
However, the RV water level (+29 inches) was greater than the desired level for opening an MSIV with-the RV pressurized. Corrective action taken-included revising Procedure 2.2.92 (to.Rev. 25) to maintain a lower initial RV water level in the " Low End" of the normalL '
operating range at less than 24"' prior to opening an MSIV.with the RV pressurized.to account for swell.
9 P
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,_a NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 n-un EXPIRES 5/31/95
. ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS LICENSEE EVENT REPORT (LER) MMfL"OunE EMOTinr%O d TEXT CONTINUATION sus *EE"$NEwaEEEo"[AE '
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FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (2)
YEAR ET MD R Sof 5 PILGRIM NUCLEAR POWER STATION 05000-293 93 - -012-- 00 TEXT (if rnore space is required, use additional copies of NRC Form 366A)(17)
For LER 89-007-00, a Group 1 isolation occurred during the power scension program on ~
February 11, 1989, at 0936 hours0.0108 days <br />0.26 hours <br />0.00155 weeks <br />3.56148e-4 months <br />. At the time of the event, the reactor power level was 0.8 percent, the reactor mode selector switch was in the STARTUP position, the RV pressure was 278 psig, and the RV water level was approximately +34 inches. The inboard MSIVs A0-203-1A/B/C/D were in the open position with the outboard MSIVs A0-203~2A/B/D in the closed position. The outboard MSIV A0-203-2C was being opened with differential pressure of approximately 150 psid in accordance with Procedure TP 87.-219 (Rev. 3), "MSIV Opening Test", step 10.5. The isolation was the result of a high RV water level (+48 inches) due to swell that occurred while opening the MSIV. The cause of the event included a procedure weakness in that the procedure did not indicate a high RV water level could occur as a result of the test and did not specify or recommend an initial RV water level for the test. Procedure TP 87-219 was subsequently retired.
ENERGY INDUSTRY IDENTIFICATION SYSTEM (EIIS) CODES The EIIS codes for this report are as follows:
COMPONENTS CODES Valve, isolation (MSIV) ISV t SYSTEMS Containment Isolation Control System (PCIS) JM Engineered Safety Features Actuation System (PCIS) JE Main Steam System SB NRC FORM 366A (5-82)
_. ,