|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046C3131993-07-28028 July 1993 LER 93-015-00:on 930630,HPCI Sys Declared Inoperable Due to Indicated Flow During Surveillance.Caused by Foreign Matl That Plugged Portion of Restricting Orifice.Restricting Orifice Removed,Cleaned & reinstalled.W/930728 Ltr ML20046B5241993-07-26026 July 1993 LER 93-007-01:on 930317,automatic Closing of RCIC Sys Turbine Steam Supply Isolation Valves Occurred Due to High Steam Flow Signal.Increased Frequency of Valve Testing from Monthly to weekly.W/930726 Ltr ML20045F8601993-06-30030 June 1993 LER 93-014-00:on 930531,automatic Scram Occurred,Resulting from Operation of Auxiliary Transformer Differential Relay During Power Ascension.Uat Phase B & C Differential Relays Left Interchanged as Investigative aid.W/930630 Ltr ML20045E2301993-06-25025 June 1993 LER 93-013-00:on 930530,RCIC Sys Declared Inoperable & 7 Day TS 3.5.D.2 LCO Entered Due to Speed Oscillations Which Occurred After Several Minutes of steady-state Operation. Caused by Actuator Failure.Actuator replaced.W/930625 Ltr ML20045E2251993-06-25025 June 1993 LER 93-012-00:on 930529,unplanned PCIS Group I Isolation Signal Occurred While Opening MSIV During Startup,Resulting in Automatic Closing of Related Valves.Caused by Licensed Operator Error.Group 1 Isolation reset.W/930625 Ltr ML20045D6941993-06-23023 June 1993 LER 93-011-00:on 930525,determined That Initial as-found Popping Pressures of Pilot Valves for Three Target Rock Main Steam Relief Valves Out of TS Tolerance.Caused by Setpoint Drift.Valves Reworked & Reassembled by Target Rock Corp ML20045D1861993-06-18018 June 1993 LER 93-010-00:on 930519,SUT Became de-energized During Planned Calibr of Turbine/Generator Relays Lockout Test While Shut Down.Caused by Personnel Error.Discussion Conducted W/Personnel Re Attention to detail.W/930618 Ltr ML20044H0441993-06-0202 June 1993 LER 93-009-00:on 930504,circuit Breaker Did Not Close During Planned Bus Transfer Due to Loose Control Circuit Wire.Lug Replaced & Reterminated on 930505 & Post Work Testing Completed W/Satisfactory results.W/930602 Ltr ML20024G7451991-04-24024 April 1991 LER 91-005-00:on 910325,diesel Generator Inoperable,Causing Loss of Ac Power to Train B Components of Safety Sys & Actuating Portions of Primary/Secondary Containment Sys. Caused by Voltage Regulator failure.W/910424 Ltr ML20029A6721991-02-25025 February 1991 LER 91-001-00:on 910125,automatic Primary Containment Isolation Control Sys Group 5 Actuation Occurred,Resulting in Closing of RCIC Turbine Steam Supply Isolation Valves. Caused by High Flow conditions.W/910225 Ltr ML20028G9731990-09-20020 September 1990 LER 89-036-01:on 891122,determined That HPCI Sys Inoperable Due to Inoperable Gland Seal Condenser Blower Motor.Caused by age-related Wear of Motor.Blower Motor Replaced & Blower Tested W/Satisfactory results.W/900920 Ltr ML20028G9121990-09-18018 September 1990 LER 89-037-01:on 891130,primary Containment/Traversing in-core Probe Ball Valve Discovered to Be Almost Full Open. Caused by Damage to Valve Stem Due to Manual Manipulation of Stem.Ball Valve & Solenoid Actuator replaced.W/900918 Ltr ML20043G3541990-06-12012 June 1990 LER 90-008-00:on 900513,automatic Scram Resulting from Load Rejection Occurred While at Full Power,Resulting in Trip of Generator Field Breakers.Caused by Fault on Offsite 345 Kv Transmission sys.Loss-of-field Relay replaced.W/900612 Ltr ML20043F8291990-06-0606 June 1990 LER 90-007-00:on 900507,discovered That Drywell to Suppression Chamber Vacuum Breaker Surveillance Not Performed Prior to Startup in 1988.Caused by Misunderstanding of requirements.W/900606 Ltr ML20042F5911990-04-30030 April 1990 LER 90-006-00:on 900330,determined That Position of Primary Containment Sys Isolation Valve Not Recorded Daily,Per Tech Specs.Review Performed to Determine If Other Problems Existed.Plant Shut Down & Review performed.W/900430 Ltr ML20012F5751990-04-0606 April 1990 LER 90-003-00:on 900311,automatic Actuation of Main Steam Sys Group 1 Portion of Primary Containment Isolation Control Sys Occurred.Caused by False High Reactor Vessel Water Level Signal.Procedure Developed Re backfill.W/900406 Ltr ML20012E9831990-03-30030 March 1990 LER 90-002-00:on 900228,determined That Max Fraction of Limiting Power Density Not Checked Daily During Reactor Power Operation,Per Tech Spec 4.1.B.On 900323,addl Tech Spec Issue Discovered.Tech Specs changed.W/900330 Ltr ML20012C4871990-03-12012 March 1990 LER 90-001-00:on 900209,24 H Limiting Condition for Operation Entered When Two RCS Instrumentation Excess Flow Check Valves Inappropriately Verified Operable During Testing.Cause Undetermined.Two Valves replaced.W/900312 Ltr ML20005G0981990-01-0808 January 1990 LER 89-038-00:on 891208,unplanned Automatic Reactor Protection Sys Scram Signal & Reactor Scram Occurred.Caused by False Low Reactor Vessel Water Level Signal.Local Level Indicators Satisfactorily calibr.W/900108 Ltr ML20005F8481990-01-0808 January 1990 LER 89-039-00:on 891209,automatic Actuation of RHR Sys Portion of Primary Containment Isolation Control Sys Occurred.Caused by Hydrodynamic Transient That Actuated Protective High Pressure switches.W/900108 Ltr ML20005E8551989-12-30030 December 1989 LER 89-037-00:on 891130,discovered That Traversing in-core Probe Ball Valve,Mfg by Consolidated Controls,Inc,Closed,In Violation of Tech Specs.Caused by Damage to Valve Stem.Ball Valve & Actuator replaced.W/891230 Ltr ML20011D1361989-12-11011 December 1989 LER 89-035-00:on 891111,inadvertent Actuation of Portion of Secondary Containment Sys During Surveillance Testing Occurred.Caused by Location of Radiation Isolation Control Sys Channel a Logic Relay.Procedure revised.W/891211 Ltr ML20005D7421989-12-0606 December 1989 LER 89-033-00:on 891106,automatic Actuation of Group 1 Portion of Primary Containment Isolation Control Sys (PCIS) Occurred.Caused by High Reactor Vessel Water Level.Manual Valve Closed & PCIS Logic Circuitry reset.W/891206 Ltr ML19351A4581989-12-0606 December 1989 LER 89-034-00:on 891108,determined That Reactor Pressure Exceeded 150 Psig on 891107 W/O Performing Surveillance Procedure 8.5.4.4, HPCI Valve Operability Test. Caused by Personnel Error.Procedure initiated.W/891206 Ltr ML19332D1421989-11-22022 November 1989 LER 89-031-00:on 891024,closing Times for Two in-series Primary Containment Isolation Valves Exceeded Acceptance Criteria During Shutdown Testing.Cause Undetermined.Closing Time Retested W/Satisfactory results.W/891122 Ltr ML19332D6231989-11-20020 November 1989 LER 89-032-00:on 891020,pneumatic Pressure Drop for Two of Four Automatic Depressurization Sys Accumulators Discovered Greater than Max Acceptable Value.Caused by Leakage from Seat of Supply Check Valves.Seat replaced.W/891120 Ltr ML19324C3181989-11-0909 November 1989 LER 88-002-01:on 880117,full Reactor Protection Sys Scram Trip Signal Occurred During Surveillance Test,Resulting in Incomplete Actuations.Caused by Procedure Inadequacy.Logic Relay Replaced & Procedure revised.W/891109 Ltr ML19324B1131989-10-21021 October 1989 LER 89-030-00:on 890926,control Room High Efficiency Air Filtration Sys Flowrate non-conservative Due to Procedure Error.Caused by Transcription Error.Procedure Revised & Test Reperformed Using Corrected procedure.W/891021 Ltr ML19325D4681989-10-16016 October 1989 LER 89-029-00:on 890914,locked High Radiation Area Door Found to Have Been Unsecured Contrary to Tech Spec 6.13.2. Caused by Failure to Adhere to Approved Procedures. Training on Access Requirements initiated.W/891016 Ltr ML19325D1861989-10-10010 October 1989 LER 89-028-00:on 890907,HPCI Sys Declared Inoperable Because Mechanical Overspeed Trip Occurred During Surveillance Test. Caused by Failure of Ramp Generator Signal Converter Module. Module Removed & Sent to Mfg for exam.W/891010 Ltr ML17277B8221984-07-20020 July 1984 LER 82-049/01X-1:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting.Caused by Personnel Error.Valve Removed & Replaced W/Properly Set Spare Valve. Procedure revised.W/840720 Ltr ML20024C3231983-06-24024 June 1983 Updated LER 82-038/03X-1:on 820817,RCIC Steam Line High Differential Pressure Alarm Received.Caused by Air in Sensing Lines to Pressure Switches.Cross Threaded Cap Found on in-line Snubber.Snubber replaced.W/830624 Ltr ML20024C2211983-06-24024 June 1983 Updated LER 80-053/03X-1:on 800814,0907 & 14,HPCI Turbine Exhaust Line Snubber 23-3-36 Determined Inoperable.Caused by Transient Hydrodynamic Shock During Startup & Shutdown. Snubbers upgraded.W/830624 Ltr ML20024B8451983-06-24024 June 1983 LER 83-031/03L-0:on 830528,HPCI Sys Made Inoperable to Repair Steam Leak on AO 2301-31.Caused by Leaking Stem Packing.Packing Replaced.Valve Tested Satisfactorily.Sys Returned to svc.W/830624 Ltr ML20024B8321983-06-24024 June 1983 LER 83-030/03L-0:on 830527,both HPCI Area Smoke Detection Sys Alarmed in Main Control Room.Caused by Valve A02301-31 Steam Leak Causing False Indications.Valve repaired.W/830624 Ltr ML20024C3101983-06-21021 June 1983 Updated LER 79-007/03X-1:on 790212,while Performing Test 8.7.4.3,valves AO-5033A,CV-5065-10,15,16 & 17 Failed to Give Proper Position Indication When Cycled & to Close within Specified Tolerance.Cause Not stated.W/830621 Ltr ML20024A8861983-06-16016 June 1983 LER 83-027/03L-0:on 830518,during Routine Insp,Folding Fire Door Found Inoperable.Caused by Operating Cable Becoming Detached from Pulley Due to Slack.Cable Reattached & Operating Mechanism adjusted.W/830616 Ltr ML20023D1691983-05-0909 May 1983 Updated LER 82-008/01X-1:on 820331,HPCI Injection Valve MO-2301-8 Failed to Open in Required Manner.Caused by Missing Wire Jumper Intended to Bypass Motor Operator Torque Switch.Jumper Installed & Valve Tested Satisfactorily ML20023D0671983-05-0909 May 1983 LER 83-021/03L-0:on 830411,during Surveillance Test 8.7.4.3, Primary Containment Isolation Valve AO-5033B Failed to Meet 10-s Closing Time Requirements.Caused by Lubricant Infiltrating Solenoid Valve Components.Components Replaced ML20023D0181983-05-0404 May 1983 LER 83-022/03L-0:on 830413,overload on Valve Motor 1301-17 Resulted in Loss of High Pressure Core Cooling Backup Capability.Caused by Oxidation in Motor End Bell & Motor Brushes,Due to Humidity Caused by Leaking Valve Packing ML20028G1591983-01-28028 January 1983 LER 83-002/01T-0:on 830116,flow Ref off-normal Alarm Received.Average Power Range Monitor Flux Scram Trip Settings Affected.Cause Under Investigation.Flow Inputs Monitored & Amplifier B Recalibr ML20028F4121983-01-17017 January 1983 LER 83-002/01X-0:on 830116,while Clearing off-normal Alarm for Flow Comparators,Average Power Range Monitor Flux Scram Trip Settings Found in Nonconservative Direction.Caused by Drifting Proportional Amplifiers.Settings Checked Daily ML20028B0421982-11-16016 November 1982 LER 82-049/01T-0:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting of 1240 Psig, Exceeding Tech Specs.Caused by Personnel Error.Set Valve Removed,Procedure Adherence Stressed & Procedure Revised ML20027C9801982-10-20020 October 1982 LER 82-039/03L-0:on 820920,timing Tests of Three Reactor Water Cleanup Isolation Valves 1201-2,-5 & -80 Not Completed within Allowed Time.Caused by Operational Constraints Requiring Testing at Reduced Power ML20027C9941982-10-20020 October 1982 LER 82-040/03L-0:on 820920,found Reactor Protection Sys Initiation Function of Turbine Stop Valve Completed 1 Day Late.Caused by Decision to Defer Test Due to MSIV D Line Isolation.Tracking Sys Implemented to Prevent Recurrences ML20052B9141982-04-23023 April 1982 LER 82-010/03L-0:on 820326,during Review of Testing Requirements,Surveillance Test 8.I.4 Standby Liquid Control Sys Found Not Verified.Caused by Breakdown in Multidiscipline Review of Results ML20052F2071982-04-14014 April 1982 Updated LER 81-060/03X-1:on 811020,determined Potential Exists to Reduce Number of Operable APRM & IRM Instrument Channels in Rod Block Trip Sys to Below Tech Spec Min ML20050A6321982-03-19019 March 1982 Updated LER 82-055/01T-1:on 810926,during Shutdown,Yarway Level Indicators Started Oscillating.Drywell Temp Was 240 F at 81-ft W/Elevation Coolant Temp 220 F.Caused by Ineffective Drywell Cooling.Ventilation Returned to Svc ML20050A4521982-03-19019 March 1982 LER 82-006/01T-0:on 820304,while Performing Maint Re SIL 352 on Pressure Adjustment Mechanism HPCI Stop Valve,Three Broken cap-screws Found.No Cause Determined.Screws Examined, Replaced & Sys Returned to Svc ML20050A4331982-03-19019 March 1982 Updated LER 81-062/01X-1:on 811116,Wyle Labs Informed Util That Two Target Rock Safety Relief Valves Had Not Passed Setpoint Tests.Caused by Setpoint Shift Due to Changes to Designed Differential Forces from Excessive Pilot Leakage 1993-07-28
[Table view] Category:RO)
MONTHYEARML20046C3131993-07-28028 July 1993 LER 93-015-00:on 930630,HPCI Sys Declared Inoperable Due to Indicated Flow During Surveillance.Caused by Foreign Matl That Plugged Portion of Restricting Orifice.Restricting Orifice Removed,Cleaned & reinstalled.W/930728 Ltr ML20046B5241993-07-26026 July 1993 LER 93-007-01:on 930317,automatic Closing of RCIC Sys Turbine Steam Supply Isolation Valves Occurred Due to High Steam Flow Signal.Increased Frequency of Valve Testing from Monthly to weekly.W/930726 Ltr ML20045F8601993-06-30030 June 1993 LER 93-014-00:on 930531,automatic Scram Occurred,Resulting from Operation of Auxiliary Transformer Differential Relay During Power Ascension.Uat Phase B & C Differential Relays Left Interchanged as Investigative aid.W/930630 Ltr ML20045E2301993-06-25025 June 1993 LER 93-013-00:on 930530,RCIC Sys Declared Inoperable & 7 Day TS 3.5.D.2 LCO Entered Due to Speed Oscillations Which Occurred After Several Minutes of steady-state Operation. Caused by Actuator Failure.Actuator replaced.W/930625 Ltr ML20045E2251993-06-25025 June 1993 LER 93-012-00:on 930529,unplanned PCIS Group I Isolation Signal Occurred While Opening MSIV During Startup,Resulting in Automatic Closing of Related Valves.Caused by Licensed Operator Error.Group 1 Isolation reset.W/930625 Ltr ML20045D6941993-06-23023 June 1993 LER 93-011-00:on 930525,determined That Initial as-found Popping Pressures of Pilot Valves for Three Target Rock Main Steam Relief Valves Out of TS Tolerance.Caused by Setpoint Drift.Valves Reworked & Reassembled by Target Rock Corp ML20045D1861993-06-18018 June 1993 LER 93-010-00:on 930519,SUT Became de-energized During Planned Calibr of Turbine/Generator Relays Lockout Test While Shut Down.Caused by Personnel Error.Discussion Conducted W/Personnel Re Attention to detail.W/930618 Ltr ML20044H0441993-06-0202 June 1993 LER 93-009-00:on 930504,circuit Breaker Did Not Close During Planned Bus Transfer Due to Loose Control Circuit Wire.Lug Replaced & Reterminated on 930505 & Post Work Testing Completed W/Satisfactory results.W/930602 Ltr ML20024G7451991-04-24024 April 1991 LER 91-005-00:on 910325,diesel Generator Inoperable,Causing Loss of Ac Power to Train B Components of Safety Sys & Actuating Portions of Primary/Secondary Containment Sys. Caused by Voltage Regulator failure.W/910424 Ltr ML20029A6721991-02-25025 February 1991 LER 91-001-00:on 910125,automatic Primary Containment Isolation Control Sys Group 5 Actuation Occurred,Resulting in Closing of RCIC Turbine Steam Supply Isolation Valves. Caused by High Flow conditions.W/910225 Ltr ML20028G9731990-09-20020 September 1990 LER 89-036-01:on 891122,determined That HPCI Sys Inoperable Due to Inoperable Gland Seal Condenser Blower Motor.Caused by age-related Wear of Motor.Blower Motor Replaced & Blower Tested W/Satisfactory results.W/900920 Ltr ML20028G9121990-09-18018 September 1990 LER 89-037-01:on 891130,primary Containment/Traversing in-core Probe Ball Valve Discovered to Be Almost Full Open. Caused by Damage to Valve Stem Due to Manual Manipulation of Stem.Ball Valve & Solenoid Actuator replaced.W/900918 Ltr ML20043G3541990-06-12012 June 1990 LER 90-008-00:on 900513,automatic Scram Resulting from Load Rejection Occurred While at Full Power,Resulting in Trip of Generator Field Breakers.Caused by Fault on Offsite 345 Kv Transmission sys.Loss-of-field Relay replaced.W/900612 Ltr ML20043F8291990-06-0606 June 1990 LER 90-007-00:on 900507,discovered That Drywell to Suppression Chamber Vacuum Breaker Surveillance Not Performed Prior to Startup in 1988.Caused by Misunderstanding of requirements.W/900606 Ltr ML20042F5911990-04-30030 April 1990 LER 90-006-00:on 900330,determined That Position of Primary Containment Sys Isolation Valve Not Recorded Daily,Per Tech Specs.Review Performed to Determine If Other Problems Existed.Plant Shut Down & Review performed.W/900430 Ltr ML20012F5751990-04-0606 April 1990 LER 90-003-00:on 900311,automatic Actuation of Main Steam Sys Group 1 Portion of Primary Containment Isolation Control Sys Occurred.Caused by False High Reactor Vessel Water Level Signal.Procedure Developed Re backfill.W/900406 Ltr ML20012E9831990-03-30030 March 1990 LER 90-002-00:on 900228,determined That Max Fraction of Limiting Power Density Not Checked Daily During Reactor Power Operation,Per Tech Spec 4.1.B.On 900323,addl Tech Spec Issue Discovered.Tech Specs changed.W/900330 Ltr ML20012C4871990-03-12012 March 1990 LER 90-001-00:on 900209,24 H Limiting Condition for Operation Entered When Two RCS Instrumentation Excess Flow Check Valves Inappropriately Verified Operable During Testing.Cause Undetermined.Two Valves replaced.W/900312 Ltr ML20005G0981990-01-0808 January 1990 LER 89-038-00:on 891208,unplanned Automatic Reactor Protection Sys Scram Signal & Reactor Scram Occurred.Caused by False Low Reactor Vessel Water Level Signal.Local Level Indicators Satisfactorily calibr.W/900108 Ltr ML20005F8481990-01-0808 January 1990 LER 89-039-00:on 891209,automatic Actuation of RHR Sys Portion of Primary Containment Isolation Control Sys Occurred.Caused by Hydrodynamic Transient That Actuated Protective High Pressure switches.W/900108 Ltr ML20005E8551989-12-30030 December 1989 LER 89-037-00:on 891130,discovered That Traversing in-core Probe Ball Valve,Mfg by Consolidated Controls,Inc,Closed,In Violation of Tech Specs.Caused by Damage to Valve Stem.Ball Valve & Actuator replaced.W/891230 Ltr ML20011D1361989-12-11011 December 1989 LER 89-035-00:on 891111,inadvertent Actuation of Portion of Secondary Containment Sys During Surveillance Testing Occurred.Caused by Location of Radiation Isolation Control Sys Channel a Logic Relay.Procedure revised.W/891211 Ltr ML20005D7421989-12-0606 December 1989 LER 89-033-00:on 891106,automatic Actuation of Group 1 Portion of Primary Containment Isolation Control Sys (PCIS) Occurred.Caused by High Reactor Vessel Water Level.Manual Valve Closed & PCIS Logic Circuitry reset.W/891206 Ltr ML19351A4581989-12-0606 December 1989 LER 89-034-00:on 891108,determined That Reactor Pressure Exceeded 150 Psig on 891107 W/O Performing Surveillance Procedure 8.5.4.4, HPCI Valve Operability Test. Caused by Personnel Error.Procedure initiated.W/891206 Ltr ML19332D1421989-11-22022 November 1989 LER 89-031-00:on 891024,closing Times for Two in-series Primary Containment Isolation Valves Exceeded Acceptance Criteria During Shutdown Testing.Cause Undetermined.Closing Time Retested W/Satisfactory results.W/891122 Ltr ML19332D6231989-11-20020 November 1989 LER 89-032-00:on 891020,pneumatic Pressure Drop for Two of Four Automatic Depressurization Sys Accumulators Discovered Greater than Max Acceptable Value.Caused by Leakage from Seat of Supply Check Valves.Seat replaced.W/891120 Ltr ML19324C3181989-11-0909 November 1989 LER 88-002-01:on 880117,full Reactor Protection Sys Scram Trip Signal Occurred During Surveillance Test,Resulting in Incomplete Actuations.Caused by Procedure Inadequacy.Logic Relay Replaced & Procedure revised.W/891109 Ltr ML19324B1131989-10-21021 October 1989 LER 89-030-00:on 890926,control Room High Efficiency Air Filtration Sys Flowrate non-conservative Due to Procedure Error.Caused by Transcription Error.Procedure Revised & Test Reperformed Using Corrected procedure.W/891021 Ltr ML19325D4681989-10-16016 October 1989 LER 89-029-00:on 890914,locked High Radiation Area Door Found to Have Been Unsecured Contrary to Tech Spec 6.13.2. Caused by Failure to Adhere to Approved Procedures. Training on Access Requirements initiated.W/891016 Ltr ML19325D1861989-10-10010 October 1989 LER 89-028-00:on 890907,HPCI Sys Declared Inoperable Because Mechanical Overspeed Trip Occurred During Surveillance Test. Caused by Failure of Ramp Generator Signal Converter Module. Module Removed & Sent to Mfg for exam.W/891010 Ltr ML17277B8221984-07-20020 July 1984 LER 82-049/01X-1:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting.Caused by Personnel Error.Valve Removed & Replaced W/Properly Set Spare Valve. Procedure revised.W/840720 Ltr ML20024C3231983-06-24024 June 1983 Updated LER 82-038/03X-1:on 820817,RCIC Steam Line High Differential Pressure Alarm Received.Caused by Air in Sensing Lines to Pressure Switches.Cross Threaded Cap Found on in-line Snubber.Snubber replaced.W/830624 Ltr ML20024C2211983-06-24024 June 1983 Updated LER 80-053/03X-1:on 800814,0907 & 14,HPCI Turbine Exhaust Line Snubber 23-3-36 Determined Inoperable.Caused by Transient Hydrodynamic Shock During Startup & Shutdown. Snubbers upgraded.W/830624 Ltr ML20024B8451983-06-24024 June 1983 LER 83-031/03L-0:on 830528,HPCI Sys Made Inoperable to Repair Steam Leak on AO 2301-31.Caused by Leaking Stem Packing.Packing Replaced.Valve Tested Satisfactorily.Sys Returned to svc.W/830624 Ltr ML20024B8321983-06-24024 June 1983 LER 83-030/03L-0:on 830527,both HPCI Area Smoke Detection Sys Alarmed in Main Control Room.Caused by Valve A02301-31 Steam Leak Causing False Indications.Valve repaired.W/830624 Ltr ML20024C3101983-06-21021 June 1983 Updated LER 79-007/03X-1:on 790212,while Performing Test 8.7.4.3,valves AO-5033A,CV-5065-10,15,16 & 17 Failed to Give Proper Position Indication When Cycled & to Close within Specified Tolerance.Cause Not stated.W/830621 Ltr ML20024A8861983-06-16016 June 1983 LER 83-027/03L-0:on 830518,during Routine Insp,Folding Fire Door Found Inoperable.Caused by Operating Cable Becoming Detached from Pulley Due to Slack.Cable Reattached & Operating Mechanism adjusted.W/830616 Ltr ML20023D1691983-05-0909 May 1983 Updated LER 82-008/01X-1:on 820331,HPCI Injection Valve MO-2301-8 Failed to Open in Required Manner.Caused by Missing Wire Jumper Intended to Bypass Motor Operator Torque Switch.Jumper Installed & Valve Tested Satisfactorily ML20023D0671983-05-0909 May 1983 LER 83-021/03L-0:on 830411,during Surveillance Test 8.7.4.3, Primary Containment Isolation Valve AO-5033B Failed to Meet 10-s Closing Time Requirements.Caused by Lubricant Infiltrating Solenoid Valve Components.Components Replaced ML20023D0181983-05-0404 May 1983 LER 83-022/03L-0:on 830413,overload on Valve Motor 1301-17 Resulted in Loss of High Pressure Core Cooling Backup Capability.Caused by Oxidation in Motor End Bell & Motor Brushes,Due to Humidity Caused by Leaking Valve Packing ML20028G1591983-01-28028 January 1983 LER 83-002/01T-0:on 830116,flow Ref off-normal Alarm Received.Average Power Range Monitor Flux Scram Trip Settings Affected.Cause Under Investigation.Flow Inputs Monitored & Amplifier B Recalibr ML20028F4121983-01-17017 January 1983 LER 83-002/01X-0:on 830116,while Clearing off-normal Alarm for Flow Comparators,Average Power Range Monitor Flux Scram Trip Settings Found in Nonconservative Direction.Caused by Drifting Proportional Amplifiers.Settings Checked Daily ML20028B0421982-11-16016 November 1982 LER 82-049/01T-0:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting of 1240 Psig, Exceeding Tech Specs.Caused by Personnel Error.Set Valve Removed,Procedure Adherence Stressed & Procedure Revised ML20027C9801982-10-20020 October 1982 LER 82-039/03L-0:on 820920,timing Tests of Three Reactor Water Cleanup Isolation Valves 1201-2,-5 & -80 Not Completed within Allowed Time.Caused by Operational Constraints Requiring Testing at Reduced Power ML20027C9941982-10-20020 October 1982 LER 82-040/03L-0:on 820920,found Reactor Protection Sys Initiation Function of Turbine Stop Valve Completed 1 Day Late.Caused by Decision to Defer Test Due to MSIV D Line Isolation.Tracking Sys Implemented to Prevent Recurrences ML20052B9141982-04-23023 April 1982 LER 82-010/03L-0:on 820326,during Review of Testing Requirements,Surveillance Test 8.I.4 Standby Liquid Control Sys Found Not Verified.Caused by Breakdown in Multidiscipline Review of Results ML20052F2071982-04-14014 April 1982 Updated LER 81-060/03X-1:on 811020,determined Potential Exists to Reduce Number of Operable APRM & IRM Instrument Channels in Rod Block Trip Sys to Below Tech Spec Min ML20050A6321982-03-19019 March 1982 Updated LER 82-055/01T-1:on 810926,during Shutdown,Yarway Level Indicators Started Oscillating.Drywell Temp Was 240 F at 81-ft W/Elevation Coolant Temp 220 F.Caused by Ineffective Drywell Cooling.Ventilation Returned to Svc ML20050A4521982-03-19019 March 1982 LER 82-006/01T-0:on 820304,while Performing Maint Re SIL 352 on Pressure Adjustment Mechanism HPCI Stop Valve,Three Broken cap-screws Found.No Cause Determined.Screws Examined, Replaced & Sys Returned to Svc ML20050A4331982-03-19019 March 1982 Updated LER 81-062/01X-1:on 811116,Wyle Labs Informed Util That Two Target Rock Safety Relief Valves Had Not Passed Setpoint Tests.Caused by Setpoint Shift Due to Changes to Designed Differential Forces from Excessive Pilot Leakage 1993-07-28
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217E3021999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Pilgrim Nuclear Station.With ML20212C2921999-09-16016 September 1999 SER Accepting Licensee Request for Relief from ASME Code Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Pilgrim Nuclear Power Station ML20216F3511999-09-0808 September 1999 ISI Summary Rept for Refuel Outage 12 at Pnps ML20216E6881999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pilgrim Nuclear Power Station.With ML20210R3401999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Pilgrim Nuclear Power Station.With ML20209C4731999-07-0707 July 1999 Addendum to SE on Proposed Transfer of Operating License & Matls License from Boston Edison Co to Entergy Nuclear Generation Co ML20209H8251999-07-0101 July 1999 Provides Commission with Evaluation of & Recommendations for Improvement in Processes Used in Staff Review & Approval of Applications for Transfer of Operating Licenses of TMI-1 & Pilgrim Station ML20209E6191999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Pilgrim Nuclear Power Station.With ML20196H2451999-06-29029 June 1999 SER Denying Licensee Proposed Alternative in Relief Request PRR-13,rev 2.Staff Determined That Proposed Alternative Provides Insufficient Info to Determine Adequacy of Scope of Implementation ML20209A8901999-06-28028 June 1999 SER Accepting Licensee Proposed Alternative to Use Code Case N-573 for Remainder of 10-year Interval Pursuant to 10CFR50.55a(a)(3)(i) ML20209B9861999-06-23023 June 1999 Rev 13A to Pilgrim Nuclear Power Station COLR for Cycle 13 ML20217N9061999-06-21021 June 1999 Rept of Changes,Tests & Experiments for Period of 970422-990621 ML20195K3431999-06-15015 June 1999 Safety Evaluation Granting Licensee Request to Use Guidance of GL 90-05 to Repair Flaws in ASME Class 3 Salt Svc Water System Piping for Plant ML20195G8231999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Pnps.With ML20207E7471999-05-27027 May 1999 Safety Evaluation Granting Request Re Reduction of IGSCC Insp of Category D Welds Due to Implementation of HWC to License DPR-35 ML20206M1971999-05-11011 May 1999 SER Accepting Request for Approval to Repair Flaws in ASME Code Class 3 Salt Svc Water Piping at Plant ML20206J6611999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Pilgrim Nuclear Power Station.With ML20205L0221999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Pilgrim Nuclear Power Station.With ML20207J5471999-03-0909 March 1999 Training Simulator,1999 4-Yr Certification Rept ML20207F9401999-03-0101 March 1999 Long Term Program Semi-Annual Rept for Pilgrim Nuclear Power Station ML20207H5451999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Pilgrim Nuclear Power Station.With ML20196E2151998-12-31031 December 1998 1998 Annual Rept for Boston Edison & Securities & Exchange Commission Form 10-K Rept.With ML20206Q2741998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Pilgrim Nuclear Power Station.With ML20197J3591998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Pilgrim Nuclear Power Station.With ML20195C9951998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Pilgrim Nuclear Power Station.With ML20154K0721998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Pilgrim Nuclear Power Station.With ML20153D3901998-09-22022 September 1998 Safety Evaluation Granting 970707 Request to Use Guidance in GL 90-05 to Repair Flaws in ASME Class 3 Salt Svc Water Sys Piping for Pilgrim Nuclear Power Station ML20197C5011998-09-0404 September 1998 Rev 12C,Pages 4 & 5 to Pilgrim Nuclear Power Station Colr ML20197C5471998-08-31031 August 1998 Rev 12C to Pilgrim Nuclear Power Station Colr ML20151W8231998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Pilgrim Nuclear Power Station.With ML20237E2251998-08-26026 August 1998 Suppl & Revs to SE for Amend 173 for Pigrim Nuclear Power Station ML20237A9941998-07-31031 July 1998 Monthly Operating Rept for Pilgrim Nuclear Power Station ML20236U8201998-07-13013 July 1998 Rev 12B to Pilgrim Nuclear Power Station COLR (Cycle 12) ML20236P0151998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Pilgrim Nuclear Power Station ML20249A3741998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Pilgrim Nuclear Power Station.W/Undated Ltr ML20247H2081998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Pilgrim Nuclear Power Station ML20207B7601998-03-31031 March 1998 Final Rept, Pilgrim Nuclear Power Station Site-Specific Offsite Radiological Emergency Preparedenss Prompt Alert & Notification System Quality Assurance Verification, Prepared for FEMA ML20216G3911998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Pilgrim Nuclear Power Station ML20216J3741998-03-19019 March 1998 Safety Evaluation Accepting Licensee Request to Evaluate Elevated Tailpipe Temp on Safety Relief Valve SRV 203-3B ML20248L2241998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Pilgrim Nuclear Station ML20202G5251998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Pilgrim Nuclear Power Station ML20236M8511997-12-31031 December 1997 1997 Annual Rept for Boston Edison & Securities & Exchange Commission Form 10-K Rept ML20198L7701997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Pilgrim Nuclear Power Station ML20203D6101997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Pilgrim Nuclear Power Station ML20202D5761997-11-0808 November 1997 1997 Evaluated Exercise BECO-LTR-97-111, Monthly Operating Rept for Oct 1997 for Pilgrim Nuclear Power Station1997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Pilgrim Nuclear Power Station ML20217D6431997-10-0101 October 1997 Safety Evaluation Granting Request for Approval to Repair Flaws in Accordance W/Gl 90-05 for ASME Class 3 SSW Piping for Pilgrim ML20217H5621997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Pilgrim Nuclear Power Station ML20216J4131997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Pilgrim Nuclear Power Station ML20210J3321997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Pilgrim Nuclear Power Station 1999-09-08
[Table view] |
Text
ma
+ .
g! ' , . ' ,
y ,
l 10 CFR-50.73
[%g% f f g
g p _ a .. ;',t V E 4...
m tg t 80S70NSDd5CW
, Pilgrim Nuclear Power Station [
t s Rocky Hill Road
+
' Plymouth, Massachusetts 02360 i
+- ,
Ralph G. Bird - .I Senior Vice President - Nuclear ,
n .t i' January 8 , 1990 !
BECo- Ltr' 90- 004 o
) .'
y !U.S. Nuclear Regul' atory Commission. ,
g Attn:' Document Control Desk 3 Hashington 0.C. 20555 Docket No. 50-293 >
License No. DPR-35 1
Dear Sir:
1 Th'e enclosed Licensee Event Report (LER) 89-039-00, " Automatic Closing of the Primary Containment System Group.3 Isolation Valves While Shutdown", is submitted
.in accordance with 10 CFR Part 50.73.
- Please do not hesitate-to contact me if there are any questions regarding this
. report. :
- e. ,
e p' j . G. Bird I
'DHE/bal t
Enclosure:
LER.89-039-00' I
- cc: Mr. Hilliam Russell k
Regional Administrator, Region I U.S. Nuclear Regulatory Commission 475 Allendale Rd.
1 King of Prussia, PA 19406
%m Sr. NRC Resident Inspector - Pilgrim Station Standard BECo LER Distribution 3 0 Q I g
d Ii lDR001170318 90010e g
r; ;.,.
ADOCK 05000293 PDC
?- j e1 I k l
p pn 30$7 U.S. NUCLE AA 9.EGULATw.Y COMM188404
- f.ftEOVED OMB NO. 31E60104
.y ,
-' 5xPia58 8"
LICENSEE EVENT REPORT (IIR)
PACILITY 98AME til . DOCKET NUMSER (2) PAGE (31 Pilcrim Ntmlonr Pnunr m e w, O l 5 l 0 l 0 l 0 l ,il o ]q 1 lOFln l q TITLE (4) -
- Automatic Closing'of~the Primary Containment System Group 3 Isolation Valves While
[i. w .+.u.-
event DATIisi ~ LER NUMeER isi RaroRT DATE 17: OTHERFAceL TitsNv0Lvt0 tel 8" F AciLsTV hAMES DOCKET NUMBERiSI MONTH DAY YEAR YEAR -
n' ' [*vL MONTH DAY YEAR m 0 15101010 1 I l
~ ~
[ 1l,2 0l 9 8 9 8l9 d 3l9 0l0 0l 1 0l8 9l0 N/A 0 l 5 l0'l 0 i 0; l-l I
? THl4 REPORT IS SUDMITTED PURfuANT TO THE REQUIREMENTS OF to CFR 5: IChec* ene er siere er the toise png) (III OPERATINO .
M00*
- N 20 402m 20404.) .0.73 eH2Hi.) 73.71:n R- 20.405deHtH0 60.3steHil 90.731sH2Het 73.71tel oe, 0i O0i n .0.isim. _
m <.im
..,ui2Hv.)
_ g,,7,g,ge,,
20 4cateH1Hdil 60,73(eH2Hil 80.73teH2HvailHA) J664
[ .g::7 4 s ., -
T' ig ,
20 406(eH1Havl 50.73teH2Hel 50.73 st(2HviHHB) 20 408(aH1 Hel ' 50.736elt2 Haul 30.73teH2Hs)
LICENGEE CONT ACT FOR THl3 LER (121 NAME TELEPHONE NUMBER ARE A CODE Douglas W. Ellis - Senior Compliance Engineer 5 10 18 71417 l- 1811 16l 0 COMPLETE ONE LINE FOR EACH COMPONENT F AILURE DESCRigED IN THis REPORT (13)
C1U$E COMPONENT O' RIPORTA E A $5 SYSTEM COMPONENT M REPORTA E .
j SYST E M T hAC-i i l 'l l I I I I I I I I I I l l l l l 1 '
l l I i 1 1 1 SUPPLEMENT AL REPORT EXPECTED 1141 MONTH DAY YEAR A 1 ) i YES fit ven. can'pteen Ex!ECTED SUOMISSION OATE) NO l l l ASSTi.ACT ILimit to H00 sonces. 4.s, enerommerety torteen eng+spece tvoewntsen kness (19l L
On December 9,1989 at 1245 hours0.0144 days <br />0.346 hours <br />0.00206 weeks <br />4.737225e-4 months <br />, an autonatic actuation of the Residual Heat Removal: System (RHRS) portion of the Primary Containment Isolation Control System
.(PCIS) occurred while shutdown. The actuation occurred when the RHRS was being L started for the shutdown cooling (SDC) mode of operation in accordance with procedure. The actuation resulted in the automatic closing of the Primary
, Containment System Group 3 (three)/SDC suction piping isolation valves.
The direct cause for the actuation was a hydrodynamic transient that actuated the protective high pressure (122 psig) switches for the SDC suction piping. The root
-cause is believed to have been some unvented air in the SDC suction piping. The air was most likely introduced into a section of the piping, while shutdown in October 1989, as a result of a valve bonnet leak and/or isolation that was subsequently conducted for valve sealing. The related accessible piping was inspected with satisfactory results. The PCIS logic circuitry was reset and the RHRS was satisfactorily put into service in the SDC mode of operation at 1501 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.711305e-4 months <br />. Corrective actions being planned include reconfiguring the existing vents in the SDC suction piping for improved venting.
-This event occurred while in hot shutdown with the reactor mode selector switch in the'SHUTD0HN position. The reactor power level was zero percent. The Reactor Vessel (RV) pressure was 5 (five) psig, and the RV water temperature was 230 degrees Fahrenheit with minor decay heat. This report is submitted in accordance with 10 CFR 50.73(a)(2)(iv) and this event posed no threat to the public health and safety.
p.
.f '
fy
[- ,
Nne p.,
'"*' ' ~
speA - .
v.s aucLtoo caoutAvony couwiesion i I LICENSEE EVENT REPORT (LER) TEXT CONTINUATION cmaovan ouc wo. mo-em EXPIRES: 8?31/t,,
4 9 ACittTY NAME 06 Docetti NUMBER (21 LIR NUMetR ist PA06(31 .
,l viaa "Otm O*,T f
Pilgrim Nuclear Power Station o l5 l0 lo lo l 2] 9 l 3 8] 9 -
0 l 3l 9 -
010 42 0F 0l 5 EVENT DESCRIPTION On December 9, 1989 at 1245 hours0.0144 days <br />0.346 hours <br />0.00206 weeks <br />4.737225e-4 months <br />, an automatic actuation of the Residual Heat-Removal System (RHRS) portion of the Primary Containment Isolation Control System I (PCIS) occurred while shutdown. The actuation occurred eight seconds after I starting the RHRS pump ' A' for the shutdown cooling (SDC) mode of operation. The i actuation resulted in the following desipaed responses:
i
- The inboard and outboard Primaty Containment System (PCS)/ Group 3 (three) l SDC suction isolation valves (MO-1001-50 and -47), in the open position, I closed automatically. l
- The RHRS pump ' A' tripped automatically because the SDC suction valves were not fully open (i.e., the valves were closing). '
Initial utility Control Room licensed operator response was to close an RHRS injection valve (MO-1001-28A) and investigate the cause for the actuation. At approximately 1445 hours0.0167 days <br />0.401 hours <br />0.00239 weeks <br />5.498225e-4 months <br />, the PCIS circuitry was reset and the SDC suction valves (M0-1001-50 and -47) were reopened. At 1501 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.711305e-4 months <br />, the RHRS pump 'A' was started and the RHRS was satisfactorily put into service in the SDC mode of operation.
Failure and Malfunction Report 89-476 was written to document the event. The NRC Operations Center was notified on December 9,1989 at 1515 hours0.0175 days <br />0.421 hours <br />0.0025 weeks <br />5.764575e-4 months <br />.
This event occurred while in hot shutdown with the reactor mode selector switch in the SHUTD0HN position. The Reactor Vessel (RV) pressure was 5 (five) psig with the RV water temperature at 230 degrees Fahrenheit. The reactor power level was zero percent.
. BACKGROUND Just prior to the event, steady state shutdown operating conditions existed. The Recirculation System pumps 'A' and 'B' were not in service. The Reactor Hater Cleanup (RHCU) System was in service. The RHRS was not in service in any of its operating modes.
A reactor scram had occurred on December 8, 1989 at 0308 hours0.00356 days <br />0.0856 hours <br />5.092593e-4 weeks <br />1.17194e-4 months <br />. While still shutdown as a result of the scram (LER 89-038-00), a management decision was made on December 9, 1989 to achieve cold shutdown in order to perform planned maintenance and testing. The core decay heat was minor. However, the RV water temperature was greater than 212 degrees Fahrenheit and the SDC mode of operation was to begin in order to achieve cold shutdown conditions.
The RHRS (Loop 'A') was subsequently configured for the SDC mode of operation in accordance with section 5.4 of procedure 2.2.19 (Rev. 32) Attachment 6 (six), "RHR Shutdown Cooling Operations". The procedural steps taken included flushing and venting the SDC suction piping downstream of the outboard isolation valve (M0-1001-47) and, similarly, the discharge piping up to the Loop 'A' injection valve M0-1001-29A that is downstream and in-series with valve MO-1001-28A. At 1236 hours0.0143 days <br />0.343 hours <br />0.00204 weeks <br />4.70298e-4 months <br />, the Recirculation System Loop 'B' pump (P-2018), in service at the time, was i
shutdown in accordance with procedure 2.2.84, " Reactor Recirculation System".
%"lJ****** _ - --
spilt Peren~ agtA U.S NUCLEQQ CEOULGionY COMMISSION
( UCENSEE EVENT REPORT (LER) TEXT CONTINUATION cmRoveo oMe no mo-om (XPIRIS: $!31eMI F ACILITY 8sA484 (U DOCKET NUMSER (26 Lin NUMetR (66 Pact (31 vtAR st ppA6 .
t] g N Pilgrim Nuclear Power Station o l5 l o l o l o l 2l 9l 3 8l 9 -
0l 3 l9 -
0l 0 0l3 or 0 l5 text w-. <. meo mmnn Prior to commencing the SDC mode of operation, a pre-evolutionary briefing was conducted in accordance with procedure 1.3.37, " Conduct of Operations". At 1244 hours0.0144 days <br />0.346 hours <br />0.00206 weeks <br />4.73342e-4 months <br />, the RHRS Loop 'A' (throttling type) injection valve MO-1001-28A was closed and the in-series injection valve MO-1001-29A was opened in accordance with procedure (2.2.19 Attachment 6 section 5.4) steps [10] and [11), respectively. The ,
SDC suction valves (MO-1001-50 and -47) were then opened in accordance with procedure step [12). The RHRS Loop 'A' pump 'A' (P-203A) was then started and ;
valve M0-1001-28A was jogged open in accordance with procedure step [13] and a flow of approximately 3200 gpm was attained approximately five seconds later. The actuation occurred approximately eight seconds after the start of the pump.
CAUSE A critique of the event was conducted on December 9,1989 in accordance with procedure 1.3.63, " Conduct of Critiques and Incident Investigations". The critique was held to determine the cause for the event and was attended by appropriate l
personnel including the operators on shift at the time of the event.
The direct cause for the actuation was a hydrodynamic transient that actuated pressure switches (PS-261-23A and -238) connected to the Recirculation System Loop
'A' pump suction piping. The SDC suction piping is connected to the Recirculation System Loop 'A' piping upstream of the Loop 'A' pump suction valve. The hydrodynamic transient probably resulted from some unvented air in the SDC suction piping. The setpoint for the pressure switches is calibrated at approximately 122 psig. The PCIS Group 3 logic circuitry is arranged as an interlock such that
. reaching the setpoint of either (or both) pressure switch results in a close signal to the related RHRS valves (MO-1001-50 and -47).
The root cause for the actuation is believed to have been some unvented air in the SDC suction piping. The air.was most likely trapped in a section of the suction piping between the inboard isolation valve (M0-1001-50) and the outboard isolation valve (M0-1001-47). The air was most likely introduced into this section of piping as a result of a valve (MO-1001-50) bonnet leak and/or isolation that was conducted for subsequent leak sealing performed while shutdown in October 1989.
CORRECTIVE ACTION i
The following corrective actions that have been taken include the following:
- Field inspection of accessible SDC suction piping located outside of primary containment (Drywell) was performed with satisfactory results.
The inspections revealed no evidence of piping damage or unusual piping movement.
e The related instrumentation, alarms, logic circuitry, and valves l
(M0-1001-50 and -47) were functionally tested on December 11, 1989 with satisfactory results. The inboard valve related testing was performed in accordance with procedure 8.M.2-1.5.4 (Rev. 10) Attachment 'A', "RHR Isolation Valve Control - Test A - Inboard". The outboard valve related testing was performed in accordance with procedure 8.M.2-1.5.5 (Rev. 11)
Attachment 'A', "RHR Isolation Valve Control - Test B - Outboard".
NQC FORM 366A
, ,t -
aosp .apa v.s. NUCLEAQ REOULOT0QY COMMISSION ?
- "'l ' LICENSEE EVENT REPORT (LER) TEXT CONTINUATION cmRovio ove No aiso-oio4 eXPlRES- t!31/B FAClLif y esAsiet til
'f
, DOCKET NUMBER (2) Lt R NUMBER (6) . PA05 (3) ;
vtaa
" W .^,6 -
"'Jo*e#
Pilgrim = Nuclear Power Station 0 l6 l 0 j o l 0 l2 l9 l 3 Sl 9 -
0l3 l9 -
0l0 44 0F 0 l5 TEXT W more asses 4 pseuseet use ashamoner WMC Fame mdW IIM Corrective Actions being planned include the following: ,
4 'The reconfiguration of existing vents that would more effectively- 3 eliminate trapped air in the SDC suction piping is part of the Long Term Plan (Item 31).
SAFETY CONSEOUENCES
-This event posed no threat to the public health and safety. '
The RHRS/SDC mode of operation has a power generation design basis only. The SDC mode-of operation functions to reduce the RV water temperature to 125 degrees Fahrenheit approximately 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br /> after a shutdown for refueling or servicing activities.
If the actuation had occurred when the decay heat generation rate was greater, a gradual increase in the RV water temperature could have occurred. However, L alternate means for heat removal are available and described in procedure 2.4.25
" Loss of Shutdown Cooling", including methods for feed and letdown using the Condensate System, RNCU System, and the Main Condenser.
L This report is submitted in accordance with 10 CFR 50.73(a)(2)(iv) because the PCIS L -
logic circuitry was actuated. The SDC mode of operation is not necessary to h mitigate the consequences of an accident. The actuation was initiated by the 122 L psig RV pressure switches (PS-261-23A and -23B). The pressure switches provide a E protective function for the SDC suction piping. The SDC suction piping, extending from the Recirculation System Loop 'A' piping up to the RHRS pumps' suction valves M0-1001-43A/B/C/D, provides a flow path for the SDC mode of operation only.
SIMILARITY TO PREVIOUS EVENTS A review was conducted of Pilgrim Station Licensee Event Reports (LERs) submitted i since January 1984. The review focused on LERs submitted in accordance with D 10 CFR 50.73(a)(2)(iv) involving the closing of the RHRS/SDC suction piping isolation valves. The review identified related events reported in LERs 50-293/87-008-01, 87-015-00, and 88-025-00.
- For LER 87-008-01, an unplanned actuation of the RHRS portion of the PCIS occurred during refueling on October'15,1987 at 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br />. The actuation resulted in the automatic closing of the isolation valves (M0-1001-50 and -47) and a temporary interruption in the SDC mode of operation. At the time of the event, the refueling cavity was flooded and the decay heat generation rate was negligible. The actuation occurred during a work task involving the installation of a new PCIS relay (16A-K69) in parallel with the inboard tripping relay (16A-K28) associated
-with PS-261-23A. The coil of relay 16A-K28 became de-energized during the installation of relay 16A-K69. The cause for the actuation was contractor electrical craft personnel error due to a deficient work plan.
' CeRC poRM 366A MI
c,
. =ne apA u.s Nuc6saa RisvoaTear coMmuio=
T'cf ~ LICENSEE EVENT REPORT (LER) TEXT CONTINUATION **aovio oes no air.o-oio.
EXPIRi$:8/3USS ,
F Acit4TV NAME tu DOCKET NUM8t 9 Q) LER NUMetR 64) PAGE (3) i vsaa "Wi So*J:
Pilgrim Nuclear Power Station o is l0 l0 l0 l 2l9 l3 8l9 --
0l3l9 --
0l0 nl5 0F n l; 1
For LER 87-015-00, actuations of the RHRS portion of the PCIS logic circuitry occurred while shutdown on December 7, 1987 at 1438 hours0.0166 days <br />0.399 hours <br />0.00238 weeks <br />5.47159e-4 months <br /> and on December 8, 1987 at 2145' hours. The December 7, 1987 actuation resulted in a temporary interruption in the SDC mode of operation. The actuation occurred while a utility I&C
. technician was installing a jumper to circuit contacts related to PS-261-23A in accordance with procedure 2.1.8.1 (Rev. 2), " Class 1 System Hydrostatic Test".
During the jumper installation, a screw became disconnected and de-energized the coil of relay 16A-K28 that resulted in the event. The cause for the actuation was procedural inadequacy in that the procedure (2.1.8.1) did not adequately identify how the jumper was to be installed and did not contain a suitable caution regarding the potential impact to the SDC mode of operation. The December 9, 1987 actuation occurred at the beginning of the hydrostatic test when the RV pressure reached the setpoint of the pressure switches (PS-261-23A/B). The actuation resulted in the automatic closing of only the inboard isolation valve (H0-1001-50) because the outboard isolation valve (H0-1001-47) was in the closed position for the portion of
.the test (2.1.8.1 Rev. 2) being conducted. The cause for the actuation was procedural inadequacy in that the procedure (2.1.8.1) did not identify all the jumpers necessary to bypass the (122 psig) interlock for the test.
For LER 88-025-00, a low RV water level occurred while shutdown on December 3, 1988 at 0304 hours0.00352 days <br />0.0844 hours <br />5.026455e-4 weeks <br />1.15672e-4 months <br />. The low RV water level that occurred (+3 inches narrow range level) resulted in actuations that included the RHRS portion of the PCIS logic circuitry.
The isolation valves (H0-1001-50 and -47), in the open position, closed automatically. The low RV water level occurred following a local leak rate test of the SDC suction isolation valves when the outboard isolation valve (H0-1001-47) was opened (with valve H0-1001-50 in the open position). The valve was opened in accordance with procedure 2.2.86 (Rev.31), " Residual Heat Removal". The opening of valve M0-1001-47 resulted in the displacement of water from the RV (via the
' Recirculation System Loop 'A' pump suction piping) to an unfilled section of the 20 inch SDC suction piping. The cause for the actuation was utility licensed operator error.- A contributing factor was a weakness in the procedure (2.2.86 Rev. 31) approved for the activity being performed.
ENERGY INDUSTRY IDENTIFICATION SYSTEM (EIIS) CODES The EIIS codes for this report are as follows:
COMPONENTS CODES Pump (P-203A) P Switch, Pressure (PS-261-23A/B) PS Valve, Isolation-(M0-1001-47 and -50) ISV L
i SYSTEMS l Engineered Safety Features Actuation System (PCIS) JE Reactor Recirculation System AD Reactor Services System (RHRS/SDC mode) CF oa m.
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ .