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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046C3131993-07-28028 July 1993 LER 93-015-00:on 930630,HPCI Sys Declared Inoperable Due to Indicated Flow During Surveillance.Caused by Foreign Matl That Plugged Portion of Restricting Orifice.Restricting Orifice Removed,Cleaned & reinstalled.W/930728 Ltr ML20046B5241993-07-26026 July 1993 LER 93-007-01:on 930317,automatic Closing of RCIC Sys Turbine Steam Supply Isolation Valves Occurred Due to High Steam Flow Signal.Increased Frequency of Valve Testing from Monthly to weekly.W/930726 Ltr ML20045F8601993-06-30030 June 1993 LER 93-014-00:on 930531,automatic Scram Occurred,Resulting from Operation of Auxiliary Transformer Differential Relay During Power Ascension.Uat Phase B & C Differential Relays Left Interchanged as Investigative aid.W/930630 Ltr ML20045E2301993-06-25025 June 1993 LER 93-013-00:on 930530,RCIC Sys Declared Inoperable & 7 Day TS 3.5.D.2 LCO Entered Due to Speed Oscillations Which Occurred After Several Minutes of steady-state Operation. Caused by Actuator Failure.Actuator replaced.W/930625 Ltr ML20045E2251993-06-25025 June 1993 LER 93-012-00:on 930529,unplanned PCIS Group I Isolation Signal Occurred While Opening MSIV During Startup,Resulting in Automatic Closing of Related Valves.Caused by Licensed Operator Error.Group 1 Isolation reset.W/930625 Ltr ML20045D6941993-06-23023 June 1993 LER 93-011-00:on 930525,determined That Initial as-found Popping Pressures of Pilot Valves for Three Target Rock Main Steam Relief Valves Out of TS Tolerance.Caused by Setpoint Drift.Valves Reworked & Reassembled by Target Rock Corp ML20045D1861993-06-18018 June 1993 LER 93-010-00:on 930519,SUT Became de-energized During Planned Calibr of Turbine/Generator Relays Lockout Test While Shut Down.Caused by Personnel Error.Discussion Conducted W/Personnel Re Attention to detail.W/930618 Ltr ML20044H0441993-06-0202 June 1993 LER 93-009-00:on 930504,circuit Breaker Did Not Close During Planned Bus Transfer Due to Loose Control Circuit Wire.Lug Replaced & Reterminated on 930505 & Post Work Testing Completed W/Satisfactory results.W/930602 Ltr ML20024G7451991-04-24024 April 1991 LER 91-005-00:on 910325,diesel Generator Inoperable,Causing Loss of Ac Power to Train B Components of Safety Sys & Actuating Portions of Primary/Secondary Containment Sys. Caused by Voltage Regulator failure.W/910424 Ltr ML20029A6721991-02-25025 February 1991 LER 91-001-00:on 910125,automatic Primary Containment Isolation Control Sys Group 5 Actuation Occurred,Resulting in Closing of RCIC Turbine Steam Supply Isolation Valves. Caused by High Flow conditions.W/910225 Ltr ML20028G9731990-09-20020 September 1990 LER 89-036-01:on 891122,determined That HPCI Sys Inoperable Due to Inoperable Gland Seal Condenser Blower Motor.Caused by age-related Wear of Motor.Blower Motor Replaced & Blower Tested W/Satisfactory results.W/900920 Ltr ML20028G9121990-09-18018 September 1990 LER 89-037-01:on 891130,primary Containment/Traversing in-core Probe Ball Valve Discovered to Be Almost Full Open. Caused by Damage to Valve Stem Due to Manual Manipulation of Stem.Ball Valve & Solenoid Actuator replaced.W/900918 Ltr ML20043G3541990-06-12012 June 1990 LER 90-008-00:on 900513,automatic Scram Resulting from Load Rejection Occurred While at Full Power,Resulting in Trip of Generator Field Breakers.Caused by Fault on Offsite 345 Kv Transmission sys.Loss-of-field Relay replaced.W/900612 Ltr ML20043F8291990-06-0606 June 1990 LER 90-007-00:on 900507,discovered That Drywell to Suppression Chamber Vacuum Breaker Surveillance Not Performed Prior to Startup in 1988.Caused by Misunderstanding of requirements.W/900606 Ltr ML20042F5911990-04-30030 April 1990 LER 90-006-00:on 900330,determined That Position of Primary Containment Sys Isolation Valve Not Recorded Daily,Per Tech Specs.Review Performed to Determine If Other Problems Existed.Plant Shut Down & Review performed.W/900430 Ltr ML20012F5751990-04-0606 April 1990 LER 90-003-00:on 900311,automatic Actuation of Main Steam Sys Group 1 Portion of Primary Containment Isolation Control Sys Occurred.Caused by False High Reactor Vessel Water Level Signal.Procedure Developed Re backfill.W/900406 Ltr ML20012E9831990-03-30030 March 1990 LER 90-002-00:on 900228,determined That Max Fraction of Limiting Power Density Not Checked Daily During Reactor Power Operation,Per Tech Spec 4.1.B.On 900323,addl Tech Spec Issue Discovered.Tech Specs changed.W/900330 Ltr ML20012C4871990-03-12012 March 1990 LER 90-001-00:on 900209,24 H Limiting Condition for Operation Entered When Two RCS Instrumentation Excess Flow Check Valves Inappropriately Verified Operable During Testing.Cause Undetermined.Two Valves replaced.W/900312 Ltr ML20005G0981990-01-0808 January 1990 LER 89-038-00:on 891208,unplanned Automatic Reactor Protection Sys Scram Signal & Reactor Scram Occurred.Caused by False Low Reactor Vessel Water Level Signal.Local Level Indicators Satisfactorily calibr.W/900108 Ltr ML20005F8481990-01-0808 January 1990 LER 89-039-00:on 891209,automatic Actuation of RHR Sys Portion of Primary Containment Isolation Control Sys Occurred.Caused by Hydrodynamic Transient That Actuated Protective High Pressure switches.W/900108 Ltr ML20005E8551989-12-30030 December 1989 LER 89-037-00:on 891130,discovered That Traversing in-core Probe Ball Valve,Mfg by Consolidated Controls,Inc,Closed,In Violation of Tech Specs.Caused by Damage to Valve Stem.Ball Valve & Actuator replaced.W/891230 Ltr ML20011D1361989-12-11011 December 1989 LER 89-035-00:on 891111,inadvertent Actuation of Portion of Secondary Containment Sys During Surveillance Testing Occurred.Caused by Location of Radiation Isolation Control Sys Channel a Logic Relay.Procedure revised.W/891211 Ltr ML20005D7421989-12-0606 December 1989 LER 89-033-00:on 891106,automatic Actuation of Group 1 Portion of Primary Containment Isolation Control Sys (PCIS) Occurred.Caused by High Reactor Vessel Water Level.Manual Valve Closed & PCIS Logic Circuitry reset.W/891206 Ltr ML19351A4581989-12-0606 December 1989 LER 89-034-00:on 891108,determined That Reactor Pressure Exceeded 150 Psig on 891107 W/O Performing Surveillance Procedure 8.5.4.4, HPCI Valve Operability Test. Caused by Personnel Error.Procedure initiated.W/891206 Ltr ML19332D1421989-11-22022 November 1989 LER 89-031-00:on 891024,closing Times for Two in-series Primary Containment Isolation Valves Exceeded Acceptance Criteria During Shutdown Testing.Cause Undetermined.Closing Time Retested W/Satisfactory results.W/891122 Ltr ML19332D6231989-11-20020 November 1989 LER 89-032-00:on 891020,pneumatic Pressure Drop for Two of Four Automatic Depressurization Sys Accumulators Discovered Greater than Max Acceptable Value.Caused by Leakage from Seat of Supply Check Valves.Seat replaced.W/891120 Ltr ML19324C3181989-11-0909 November 1989 LER 88-002-01:on 880117,full Reactor Protection Sys Scram Trip Signal Occurred During Surveillance Test,Resulting in Incomplete Actuations.Caused by Procedure Inadequacy.Logic Relay Replaced & Procedure revised.W/891109 Ltr ML19324B1131989-10-21021 October 1989 LER 89-030-00:on 890926,control Room High Efficiency Air Filtration Sys Flowrate non-conservative Due to Procedure Error.Caused by Transcription Error.Procedure Revised & Test Reperformed Using Corrected procedure.W/891021 Ltr ML19325D4681989-10-16016 October 1989 LER 89-029-00:on 890914,locked High Radiation Area Door Found to Have Been Unsecured Contrary to Tech Spec 6.13.2. Caused by Failure to Adhere to Approved Procedures. Training on Access Requirements initiated.W/891016 Ltr ML19325D1861989-10-10010 October 1989 LER 89-028-00:on 890907,HPCI Sys Declared Inoperable Because Mechanical Overspeed Trip Occurred During Surveillance Test. Caused by Failure of Ramp Generator Signal Converter Module. Module Removed & Sent to Mfg for exam.W/891010 Ltr ML17277B8221984-07-20020 July 1984 LER 82-049/01X-1:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting.Caused by Personnel Error.Valve Removed & Replaced W/Properly Set Spare Valve. Procedure revised.W/840720 Ltr ML20024C3231983-06-24024 June 1983 Updated LER 82-038/03X-1:on 820817,RCIC Steam Line High Differential Pressure Alarm Received.Caused by Air in Sensing Lines to Pressure Switches.Cross Threaded Cap Found on in-line Snubber.Snubber replaced.W/830624 Ltr ML20024C2211983-06-24024 June 1983 Updated LER 80-053/03X-1:on 800814,0907 & 14,HPCI Turbine Exhaust Line Snubber 23-3-36 Determined Inoperable.Caused by Transient Hydrodynamic Shock During Startup & Shutdown. Snubbers upgraded.W/830624 Ltr ML20024B8451983-06-24024 June 1983 LER 83-031/03L-0:on 830528,HPCI Sys Made Inoperable to Repair Steam Leak on AO 2301-31.Caused by Leaking Stem Packing.Packing Replaced.Valve Tested Satisfactorily.Sys Returned to svc.W/830624 Ltr ML20024B8321983-06-24024 June 1983 LER 83-030/03L-0:on 830527,both HPCI Area Smoke Detection Sys Alarmed in Main Control Room.Caused by Valve A02301-31 Steam Leak Causing False Indications.Valve repaired.W/830624 Ltr ML20024C3101983-06-21021 June 1983 Updated LER 79-007/03X-1:on 790212,while Performing Test 8.7.4.3,valves AO-5033A,CV-5065-10,15,16 & 17 Failed to Give Proper Position Indication When Cycled & to Close within Specified Tolerance.Cause Not stated.W/830621 Ltr ML20024A8861983-06-16016 June 1983 LER 83-027/03L-0:on 830518,during Routine Insp,Folding Fire Door Found Inoperable.Caused by Operating Cable Becoming Detached from Pulley Due to Slack.Cable Reattached & Operating Mechanism adjusted.W/830616 Ltr ML20023D1691983-05-0909 May 1983 Updated LER 82-008/01X-1:on 820331,HPCI Injection Valve MO-2301-8 Failed to Open in Required Manner.Caused by Missing Wire Jumper Intended to Bypass Motor Operator Torque Switch.Jumper Installed & Valve Tested Satisfactorily ML20023D0671983-05-0909 May 1983 LER 83-021/03L-0:on 830411,during Surveillance Test 8.7.4.3, Primary Containment Isolation Valve AO-5033B Failed to Meet 10-s Closing Time Requirements.Caused by Lubricant Infiltrating Solenoid Valve Components.Components Replaced ML20023D0181983-05-0404 May 1983 LER 83-022/03L-0:on 830413,overload on Valve Motor 1301-17 Resulted in Loss of High Pressure Core Cooling Backup Capability.Caused by Oxidation in Motor End Bell & Motor Brushes,Due to Humidity Caused by Leaking Valve Packing ML20028G1591983-01-28028 January 1983 LER 83-002/01T-0:on 830116,flow Ref off-normal Alarm Received.Average Power Range Monitor Flux Scram Trip Settings Affected.Cause Under Investigation.Flow Inputs Monitored & Amplifier B Recalibr ML20028F4121983-01-17017 January 1983 LER 83-002/01X-0:on 830116,while Clearing off-normal Alarm for Flow Comparators,Average Power Range Monitor Flux Scram Trip Settings Found in Nonconservative Direction.Caused by Drifting Proportional Amplifiers.Settings Checked Daily ML20028B0421982-11-16016 November 1982 LER 82-049/01T-0:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting of 1240 Psig, Exceeding Tech Specs.Caused by Personnel Error.Set Valve Removed,Procedure Adherence Stressed & Procedure Revised ML20027C9801982-10-20020 October 1982 LER 82-039/03L-0:on 820920,timing Tests of Three Reactor Water Cleanup Isolation Valves 1201-2,-5 & -80 Not Completed within Allowed Time.Caused by Operational Constraints Requiring Testing at Reduced Power ML20027C9941982-10-20020 October 1982 LER 82-040/03L-0:on 820920,found Reactor Protection Sys Initiation Function of Turbine Stop Valve Completed 1 Day Late.Caused by Decision to Defer Test Due to MSIV D Line Isolation.Tracking Sys Implemented to Prevent Recurrences ML20052B9141982-04-23023 April 1982 LER 82-010/03L-0:on 820326,during Review of Testing Requirements,Surveillance Test 8.I.4 Standby Liquid Control Sys Found Not Verified.Caused by Breakdown in Multidiscipline Review of Results ML20052F2071982-04-14014 April 1982 Updated LER 81-060/03X-1:on 811020,determined Potential Exists to Reduce Number of Operable APRM & IRM Instrument Channels in Rod Block Trip Sys to Below Tech Spec Min ML20050A6321982-03-19019 March 1982 Updated LER 82-055/01T-1:on 810926,during Shutdown,Yarway Level Indicators Started Oscillating.Drywell Temp Was 240 F at 81-ft W/Elevation Coolant Temp 220 F.Caused by Ineffective Drywell Cooling.Ventilation Returned to Svc ML20050A4521982-03-19019 March 1982 LER 82-006/01T-0:on 820304,while Performing Maint Re SIL 352 on Pressure Adjustment Mechanism HPCI Stop Valve,Three Broken cap-screws Found.No Cause Determined.Screws Examined, Replaced & Sys Returned to Svc ML20050A4331982-03-19019 March 1982 Updated LER 81-062/01X-1:on 811116,Wyle Labs Informed Util That Two Target Rock Safety Relief Valves Had Not Passed Setpoint Tests.Caused by Setpoint Shift Due to Changes to Designed Differential Forces from Excessive Pilot Leakage 1993-07-28
[Table view] Category:RO)
MONTHYEARML20046C3131993-07-28028 July 1993 LER 93-015-00:on 930630,HPCI Sys Declared Inoperable Due to Indicated Flow During Surveillance.Caused by Foreign Matl That Plugged Portion of Restricting Orifice.Restricting Orifice Removed,Cleaned & reinstalled.W/930728 Ltr ML20046B5241993-07-26026 July 1993 LER 93-007-01:on 930317,automatic Closing of RCIC Sys Turbine Steam Supply Isolation Valves Occurred Due to High Steam Flow Signal.Increased Frequency of Valve Testing from Monthly to weekly.W/930726 Ltr ML20045F8601993-06-30030 June 1993 LER 93-014-00:on 930531,automatic Scram Occurred,Resulting from Operation of Auxiliary Transformer Differential Relay During Power Ascension.Uat Phase B & C Differential Relays Left Interchanged as Investigative aid.W/930630 Ltr ML20045E2301993-06-25025 June 1993 LER 93-013-00:on 930530,RCIC Sys Declared Inoperable & 7 Day TS 3.5.D.2 LCO Entered Due to Speed Oscillations Which Occurred After Several Minutes of steady-state Operation. Caused by Actuator Failure.Actuator replaced.W/930625 Ltr ML20045E2251993-06-25025 June 1993 LER 93-012-00:on 930529,unplanned PCIS Group I Isolation Signal Occurred While Opening MSIV During Startup,Resulting in Automatic Closing of Related Valves.Caused by Licensed Operator Error.Group 1 Isolation reset.W/930625 Ltr ML20045D6941993-06-23023 June 1993 LER 93-011-00:on 930525,determined That Initial as-found Popping Pressures of Pilot Valves for Three Target Rock Main Steam Relief Valves Out of TS Tolerance.Caused by Setpoint Drift.Valves Reworked & Reassembled by Target Rock Corp ML20045D1861993-06-18018 June 1993 LER 93-010-00:on 930519,SUT Became de-energized During Planned Calibr of Turbine/Generator Relays Lockout Test While Shut Down.Caused by Personnel Error.Discussion Conducted W/Personnel Re Attention to detail.W/930618 Ltr ML20044H0441993-06-0202 June 1993 LER 93-009-00:on 930504,circuit Breaker Did Not Close During Planned Bus Transfer Due to Loose Control Circuit Wire.Lug Replaced & Reterminated on 930505 & Post Work Testing Completed W/Satisfactory results.W/930602 Ltr ML20024G7451991-04-24024 April 1991 LER 91-005-00:on 910325,diesel Generator Inoperable,Causing Loss of Ac Power to Train B Components of Safety Sys & Actuating Portions of Primary/Secondary Containment Sys. Caused by Voltage Regulator failure.W/910424 Ltr ML20029A6721991-02-25025 February 1991 LER 91-001-00:on 910125,automatic Primary Containment Isolation Control Sys Group 5 Actuation Occurred,Resulting in Closing of RCIC Turbine Steam Supply Isolation Valves. Caused by High Flow conditions.W/910225 Ltr ML20028G9731990-09-20020 September 1990 LER 89-036-01:on 891122,determined That HPCI Sys Inoperable Due to Inoperable Gland Seal Condenser Blower Motor.Caused by age-related Wear of Motor.Blower Motor Replaced & Blower Tested W/Satisfactory results.W/900920 Ltr ML20028G9121990-09-18018 September 1990 LER 89-037-01:on 891130,primary Containment/Traversing in-core Probe Ball Valve Discovered to Be Almost Full Open. Caused by Damage to Valve Stem Due to Manual Manipulation of Stem.Ball Valve & Solenoid Actuator replaced.W/900918 Ltr ML20043G3541990-06-12012 June 1990 LER 90-008-00:on 900513,automatic Scram Resulting from Load Rejection Occurred While at Full Power,Resulting in Trip of Generator Field Breakers.Caused by Fault on Offsite 345 Kv Transmission sys.Loss-of-field Relay replaced.W/900612 Ltr ML20043F8291990-06-0606 June 1990 LER 90-007-00:on 900507,discovered That Drywell to Suppression Chamber Vacuum Breaker Surveillance Not Performed Prior to Startup in 1988.Caused by Misunderstanding of requirements.W/900606 Ltr ML20042F5911990-04-30030 April 1990 LER 90-006-00:on 900330,determined That Position of Primary Containment Sys Isolation Valve Not Recorded Daily,Per Tech Specs.Review Performed to Determine If Other Problems Existed.Plant Shut Down & Review performed.W/900430 Ltr ML20012F5751990-04-0606 April 1990 LER 90-003-00:on 900311,automatic Actuation of Main Steam Sys Group 1 Portion of Primary Containment Isolation Control Sys Occurred.Caused by False High Reactor Vessel Water Level Signal.Procedure Developed Re backfill.W/900406 Ltr ML20012E9831990-03-30030 March 1990 LER 90-002-00:on 900228,determined That Max Fraction of Limiting Power Density Not Checked Daily During Reactor Power Operation,Per Tech Spec 4.1.B.On 900323,addl Tech Spec Issue Discovered.Tech Specs changed.W/900330 Ltr ML20012C4871990-03-12012 March 1990 LER 90-001-00:on 900209,24 H Limiting Condition for Operation Entered When Two RCS Instrumentation Excess Flow Check Valves Inappropriately Verified Operable During Testing.Cause Undetermined.Two Valves replaced.W/900312 Ltr ML20005G0981990-01-0808 January 1990 LER 89-038-00:on 891208,unplanned Automatic Reactor Protection Sys Scram Signal & Reactor Scram Occurred.Caused by False Low Reactor Vessel Water Level Signal.Local Level Indicators Satisfactorily calibr.W/900108 Ltr ML20005F8481990-01-0808 January 1990 LER 89-039-00:on 891209,automatic Actuation of RHR Sys Portion of Primary Containment Isolation Control Sys Occurred.Caused by Hydrodynamic Transient That Actuated Protective High Pressure switches.W/900108 Ltr ML20005E8551989-12-30030 December 1989 LER 89-037-00:on 891130,discovered That Traversing in-core Probe Ball Valve,Mfg by Consolidated Controls,Inc,Closed,In Violation of Tech Specs.Caused by Damage to Valve Stem.Ball Valve & Actuator replaced.W/891230 Ltr ML20011D1361989-12-11011 December 1989 LER 89-035-00:on 891111,inadvertent Actuation of Portion of Secondary Containment Sys During Surveillance Testing Occurred.Caused by Location of Radiation Isolation Control Sys Channel a Logic Relay.Procedure revised.W/891211 Ltr ML20005D7421989-12-0606 December 1989 LER 89-033-00:on 891106,automatic Actuation of Group 1 Portion of Primary Containment Isolation Control Sys (PCIS) Occurred.Caused by High Reactor Vessel Water Level.Manual Valve Closed & PCIS Logic Circuitry reset.W/891206 Ltr ML19351A4581989-12-0606 December 1989 LER 89-034-00:on 891108,determined That Reactor Pressure Exceeded 150 Psig on 891107 W/O Performing Surveillance Procedure 8.5.4.4, HPCI Valve Operability Test. Caused by Personnel Error.Procedure initiated.W/891206 Ltr ML19332D1421989-11-22022 November 1989 LER 89-031-00:on 891024,closing Times for Two in-series Primary Containment Isolation Valves Exceeded Acceptance Criteria During Shutdown Testing.Cause Undetermined.Closing Time Retested W/Satisfactory results.W/891122 Ltr ML19332D6231989-11-20020 November 1989 LER 89-032-00:on 891020,pneumatic Pressure Drop for Two of Four Automatic Depressurization Sys Accumulators Discovered Greater than Max Acceptable Value.Caused by Leakage from Seat of Supply Check Valves.Seat replaced.W/891120 Ltr ML19324C3181989-11-0909 November 1989 LER 88-002-01:on 880117,full Reactor Protection Sys Scram Trip Signal Occurred During Surveillance Test,Resulting in Incomplete Actuations.Caused by Procedure Inadequacy.Logic Relay Replaced & Procedure revised.W/891109 Ltr ML19324B1131989-10-21021 October 1989 LER 89-030-00:on 890926,control Room High Efficiency Air Filtration Sys Flowrate non-conservative Due to Procedure Error.Caused by Transcription Error.Procedure Revised & Test Reperformed Using Corrected procedure.W/891021 Ltr ML19325D4681989-10-16016 October 1989 LER 89-029-00:on 890914,locked High Radiation Area Door Found to Have Been Unsecured Contrary to Tech Spec 6.13.2. Caused by Failure to Adhere to Approved Procedures. Training on Access Requirements initiated.W/891016 Ltr ML19325D1861989-10-10010 October 1989 LER 89-028-00:on 890907,HPCI Sys Declared Inoperable Because Mechanical Overspeed Trip Occurred During Surveillance Test. Caused by Failure of Ramp Generator Signal Converter Module. Module Removed & Sent to Mfg for exam.W/891010 Ltr ML17277B8221984-07-20020 July 1984 LER 82-049/01X-1:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting.Caused by Personnel Error.Valve Removed & Replaced W/Properly Set Spare Valve. Procedure revised.W/840720 Ltr ML20024C3231983-06-24024 June 1983 Updated LER 82-038/03X-1:on 820817,RCIC Steam Line High Differential Pressure Alarm Received.Caused by Air in Sensing Lines to Pressure Switches.Cross Threaded Cap Found on in-line Snubber.Snubber replaced.W/830624 Ltr ML20024C2211983-06-24024 June 1983 Updated LER 80-053/03X-1:on 800814,0907 & 14,HPCI Turbine Exhaust Line Snubber 23-3-36 Determined Inoperable.Caused by Transient Hydrodynamic Shock During Startup & Shutdown. Snubbers upgraded.W/830624 Ltr ML20024B8451983-06-24024 June 1983 LER 83-031/03L-0:on 830528,HPCI Sys Made Inoperable to Repair Steam Leak on AO 2301-31.Caused by Leaking Stem Packing.Packing Replaced.Valve Tested Satisfactorily.Sys Returned to svc.W/830624 Ltr ML20024B8321983-06-24024 June 1983 LER 83-030/03L-0:on 830527,both HPCI Area Smoke Detection Sys Alarmed in Main Control Room.Caused by Valve A02301-31 Steam Leak Causing False Indications.Valve repaired.W/830624 Ltr ML20024C3101983-06-21021 June 1983 Updated LER 79-007/03X-1:on 790212,while Performing Test 8.7.4.3,valves AO-5033A,CV-5065-10,15,16 & 17 Failed to Give Proper Position Indication When Cycled & to Close within Specified Tolerance.Cause Not stated.W/830621 Ltr ML20024A8861983-06-16016 June 1983 LER 83-027/03L-0:on 830518,during Routine Insp,Folding Fire Door Found Inoperable.Caused by Operating Cable Becoming Detached from Pulley Due to Slack.Cable Reattached & Operating Mechanism adjusted.W/830616 Ltr ML20023D1691983-05-0909 May 1983 Updated LER 82-008/01X-1:on 820331,HPCI Injection Valve MO-2301-8 Failed to Open in Required Manner.Caused by Missing Wire Jumper Intended to Bypass Motor Operator Torque Switch.Jumper Installed & Valve Tested Satisfactorily ML20023D0671983-05-0909 May 1983 LER 83-021/03L-0:on 830411,during Surveillance Test 8.7.4.3, Primary Containment Isolation Valve AO-5033B Failed to Meet 10-s Closing Time Requirements.Caused by Lubricant Infiltrating Solenoid Valve Components.Components Replaced ML20023D0181983-05-0404 May 1983 LER 83-022/03L-0:on 830413,overload on Valve Motor 1301-17 Resulted in Loss of High Pressure Core Cooling Backup Capability.Caused by Oxidation in Motor End Bell & Motor Brushes,Due to Humidity Caused by Leaking Valve Packing ML20028G1591983-01-28028 January 1983 LER 83-002/01T-0:on 830116,flow Ref off-normal Alarm Received.Average Power Range Monitor Flux Scram Trip Settings Affected.Cause Under Investigation.Flow Inputs Monitored & Amplifier B Recalibr ML20028F4121983-01-17017 January 1983 LER 83-002/01X-0:on 830116,while Clearing off-normal Alarm for Flow Comparators,Average Power Range Monitor Flux Scram Trip Settings Found in Nonconservative Direction.Caused by Drifting Proportional Amplifiers.Settings Checked Daily ML20028B0421982-11-16016 November 1982 LER 82-049/01T-0:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting of 1240 Psig, Exceeding Tech Specs.Caused by Personnel Error.Set Valve Removed,Procedure Adherence Stressed & Procedure Revised ML20027C9801982-10-20020 October 1982 LER 82-039/03L-0:on 820920,timing Tests of Three Reactor Water Cleanup Isolation Valves 1201-2,-5 & -80 Not Completed within Allowed Time.Caused by Operational Constraints Requiring Testing at Reduced Power ML20027C9941982-10-20020 October 1982 LER 82-040/03L-0:on 820920,found Reactor Protection Sys Initiation Function of Turbine Stop Valve Completed 1 Day Late.Caused by Decision to Defer Test Due to MSIV D Line Isolation.Tracking Sys Implemented to Prevent Recurrences ML20052B9141982-04-23023 April 1982 LER 82-010/03L-0:on 820326,during Review of Testing Requirements,Surveillance Test 8.I.4 Standby Liquid Control Sys Found Not Verified.Caused by Breakdown in Multidiscipline Review of Results ML20052F2071982-04-14014 April 1982 Updated LER 81-060/03X-1:on 811020,determined Potential Exists to Reduce Number of Operable APRM & IRM Instrument Channels in Rod Block Trip Sys to Below Tech Spec Min ML20050A6321982-03-19019 March 1982 Updated LER 82-055/01T-1:on 810926,during Shutdown,Yarway Level Indicators Started Oscillating.Drywell Temp Was 240 F at 81-ft W/Elevation Coolant Temp 220 F.Caused by Ineffective Drywell Cooling.Ventilation Returned to Svc ML20050A4521982-03-19019 March 1982 LER 82-006/01T-0:on 820304,while Performing Maint Re SIL 352 on Pressure Adjustment Mechanism HPCI Stop Valve,Three Broken cap-screws Found.No Cause Determined.Screws Examined, Replaced & Sys Returned to Svc ML20050A4331982-03-19019 March 1982 Updated LER 81-062/01X-1:on 811116,Wyle Labs Informed Util That Two Target Rock Safety Relief Valves Had Not Passed Setpoint Tests.Caused by Setpoint Shift Due to Changes to Designed Differential Forces from Excessive Pilot Leakage 1993-07-28
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217E3021999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Pilgrim Nuclear Station.With ML20212C2921999-09-16016 September 1999 SER Accepting Licensee Request for Relief from ASME Code Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Pilgrim Nuclear Power Station ML20216F3511999-09-0808 September 1999 ISI Summary Rept for Refuel Outage 12 at Pnps ML20216E6881999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pilgrim Nuclear Power Station.With ML20210R3401999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Pilgrim Nuclear Power Station.With ML20209C4731999-07-0707 July 1999 Addendum to SE on Proposed Transfer of Operating License & Matls License from Boston Edison Co to Entergy Nuclear Generation Co ML20209H8251999-07-0101 July 1999 Provides Commission with Evaluation of & Recommendations for Improvement in Processes Used in Staff Review & Approval of Applications for Transfer of Operating Licenses of TMI-1 & Pilgrim Station ML20209E6191999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Pilgrim Nuclear Power Station.With ML20196H2451999-06-29029 June 1999 SER Denying Licensee Proposed Alternative in Relief Request PRR-13,rev 2.Staff Determined That Proposed Alternative Provides Insufficient Info to Determine Adequacy of Scope of Implementation ML20209A8901999-06-28028 June 1999 SER Accepting Licensee Proposed Alternative to Use Code Case N-573 for Remainder of 10-year Interval Pursuant to 10CFR50.55a(a)(3)(i) ML20209B9861999-06-23023 June 1999 Rev 13A to Pilgrim Nuclear Power Station COLR for Cycle 13 ML20217N9061999-06-21021 June 1999 Rept of Changes,Tests & Experiments for Period of 970422-990621 ML20195K3431999-06-15015 June 1999 Safety Evaluation Granting Licensee Request to Use Guidance of GL 90-05 to Repair Flaws in ASME Class 3 Salt Svc Water System Piping for Plant ML20195G8231999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Pnps.With ML20207E7471999-05-27027 May 1999 Safety Evaluation Granting Request Re Reduction of IGSCC Insp of Category D Welds Due to Implementation of HWC to License DPR-35 ML20206M1971999-05-11011 May 1999 SER Accepting Request for Approval to Repair Flaws in ASME Code Class 3 Salt Svc Water Piping at Plant ML20206J6611999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Pilgrim Nuclear Power Station.With ML20205L0221999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Pilgrim Nuclear Power Station.With ML20207J5471999-03-0909 March 1999 Training Simulator,1999 4-Yr Certification Rept ML20207F9401999-03-0101 March 1999 Long Term Program Semi-Annual Rept for Pilgrim Nuclear Power Station ML20207H5451999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Pilgrim Nuclear Power Station.With ML20196E2151998-12-31031 December 1998 1998 Annual Rept for Boston Edison & Securities & Exchange Commission Form 10-K Rept.With ML20206Q2741998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Pilgrim Nuclear Power Station.With ML20197J3591998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Pilgrim Nuclear Power Station.With ML20195C9951998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Pilgrim Nuclear Power Station.With ML20154K0721998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Pilgrim Nuclear Power Station.With ML20153D3901998-09-22022 September 1998 Safety Evaluation Granting 970707 Request to Use Guidance in GL 90-05 to Repair Flaws in ASME Class 3 Salt Svc Water Sys Piping for Pilgrim Nuclear Power Station ML20197C5011998-09-0404 September 1998 Rev 12C,Pages 4 & 5 to Pilgrim Nuclear Power Station Colr ML20197C5471998-08-31031 August 1998 Rev 12C to Pilgrim Nuclear Power Station Colr ML20151W8231998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Pilgrim Nuclear Power Station.With ML20237E2251998-08-26026 August 1998 Suppl & Revs to SE for Amend 173 for Pigrim Nuclear Power Station ML20237A9941998-07-31031 July 1998 Monthly Operating Rept for Pilgrim Nuclear Power Station ML20236U8201998-07-13013 July 1998 Rev 12B to Pilgrim Nuclear Power Station COLR (Cycle 12) ML20236P0151998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Pilgrim Nuclear Power Station ML20249A3741998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Pilgrim Nuclear Power Station.W/Undated Ltr ML20247H2081998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Pilgrim Nuclear Power Station ML20207B7601998-03-31031 March 1998 Final Rept, Pilgrim Nuclear Power Station Site-Specific Offsite Radiological Emergency Preparedenss Prompt Alert & Notification System Quality Assurance Verification, Prepared for FEMA ML20216G3911998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Pilgrim Nuclear Power Station ML20216J3741998-03-19019 March 1998 Safety Evaluation Accepting Licensee Request to Evaluate Elevated Tailpipe Temp on Safety Relief Valve SRV 203-3B ML20248L2241998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Pilgrim Nuclear Station ML20202G5251998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Pilgrim Nuclear Power Station ML20236M8511997-12-31031 December 1997 1997 Annual Rept for Boston Edison & Securities & Exchange Commission Form 10-K Rept ML20198L7701997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Pilgrim Nuclear Power Station ML20203D6101997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Pilgrim Nuclear Power Station ML20202D5761997-11-0808 November 1997 1997 Evaluated Exercise BECO-LTR-97-111, Monthly Operating Rept for Oct 1997 for Pilgrim Nuclear Power Station1997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Pilgrim Nuclear Power Station ML20217D6431997-10-0101 October 1997 Safety Evaluation Granting Request for Approval to Repair Flaws in Accordance W/Gl 90-05 for ASME Class 3 SSW Piping for Pilgrim ML20217H5621997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Pilgrim Nuclear Power Station ML20216J4131997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Pilgrim Nuclear Power Station ML20210J3321997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Pilgrim Nuclear Power Station 1999-09-08
[Table view] |
Text
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10 CFR 50.73 c
g, m k Pilgrim Nuclear Power station
' Rocky Hill Road '
Plymouth, Massachusetts 02360 June 12, 1990 bl hP G. Bird BECo Ltr.90-074 Senior Vice President - Nuclear U.S. Nuclear Regulatory Commission ,
Attn: Document Cont ol Desk '
Hashington,'D.C. 20555 a
Docket No. 50-293 i License No. DPR-35 l
Dear Sir:
i The enclosed-Licensee Event Report (LER) 90-006-00, " Automatic Scram Resulting {
From Load Rejection at Full Power", is submitted in accordance with 10 CFR a
Part 50.73. !
- Please 'do' not hesitate to contact me if there are any questions regarding this report. j) l Ya h 1
DHE/bal l
Enclosure:
LER 90-008 q cc:' Mr. Thomas T. Martin
% Regional' Administrator, Region I-U.S. Nuclear Regulatory Commission 4 475 Allendale Rd. h King of-Prussia,'PA4 19406 :
1 Sr. NRC Resident-Inspector --Filgrim Station i Standard BECo LER ' Distribution p l u <
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LICENSEE EVENT REPORT (LER) "aES "
P1CILITY NAM nl DOCILEY NUMOtR til PAGE (3i Pilgrim Nuclear Power Station 016101010121 911 1 loFl 018 ft1LE4' Automatic Scram Resulting From Load Rejection At Full Power EVENT DAf f (El LtR NuMetR tt) REPORT DAf t (7) OTHf R F ACILITits INv0Lvt0 let '
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t On May 13,1990 at 1603 hours0.0186 days <br />0.445 hours <br />0.00265 weeks <br />6.099415e-4 months <br />, an automatic scram resulting from a load rejection occurred while at 100 percent reactor power. The load rejection included a trip of the Generator Field Breaker, actuation of the Turbine mechanical hydraulic control speed governor, closure of the four Turbine Control Valves and opening of the three Bypass Valves, and the brief actuation of the Main Steam / Target Rock two-stage .
relief valves at approximately 1100 psig (low end of the 1115 psig setpoint range including tolerance).
The load rejection was caused by a momentary fault on the offsite 345 KV transmission system. The Generator's loss-of-field relay (240) detected the fault' and immediately tripped the Generator without an expected (inherent) 15 cycle time delay because one of it's components, the telephone relay ('X') coil, was defective. The relay (240) was last calibrated and functionally tested on October 26, 1989. At that time, the operation of the ('X') coil was tested in accordance with the vendor manual. The relay's- time delay was built-in and not adjustable, and was not required to be timed. The. relay was installed during plant construction (c. 1972). The cause for the open coil is being investigated but is believed to be random or age related failure. The relay is the only one of its type (Westinghouse type KLF-1) installed at Pilgrim Station and was replaced with another KLF-1 relay having an adjustable time delay. The (240) relay's calibration sheet was revised to. include a calibration of the adjustable time delay.
This event occurred with the reactor mode selector switch in the RUN position. The Reactor Vessel (RV) pressure was initially at 1035 psig with RV water temperature at 548 degrees Fahrenheit. This report is submitted in accordance with 10 CFR 50 73(a)(2)(iv) and this event posed no threat to the public health and safety.
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On May 13, 1990 at 1603 hours0.0186 days <br />0.445 hours <br />0.00265 weeks <br />6.099415e-4 months <br />, an unplanned automatic Reactor Protection System (RPS) scram signal and reactor scram occurred while at 100 percent reactor power.
The scram signal occurred as a result of a load rejection that included a trip of the Turbine-Generator. 4
'The t' rip of the Generator lockout' relay (286-1) resulted in the following designed' responses:
- Automatic opening of the Generator Field Breaker (41M). I l
- Automatic opening of the 345 KV switchyard air circuit breakers ACB-104 (352-4) and ACB-105 (352-5).
- Automatic transfer-of the source of 4160 VAC power for the Auxiliary Power Distribution System (APDS) from the Unit Auxiliary Transformer (UAT) to the l Startup Transformer (SUT). ;
- Automatic trip of the Turbine master trip solenoid (MTS-1) that resulted in the closing of the Turbine Stop Valves and Combined Intermediate Valves, and the-trip of'the Turbine lockout relay (286-2).
Concurrently, the Generator trip resulted in a momentary increase in Turbine speed
.that was caused by the sudden mismatch in Generator load (zero percent) and Turbine '
power (100 percent). The rapid acceleration actuated the mechanical speed governor
'in the Mechanical Hydraulic Control (MHC) portion of the Turbine Control System, and an adjustment in the mechanical linkage connected to the acceleration relay. 1 The actuation of the acceleration relay resulted in the following designed responses:
1
- ' Fast closure of-the 4 (four) Turbine Control _ Valves and the subsequent opening of the 3 (three) Turbine Bypass Valves.
,-
L .
l . The Main Steam /RV pressure increased as a result of the fast closure of the Turbine !
Control Valves. The opening of the Bypass Valves, controlled by the pressure Jregulator, mitigates the pressure transient; however, the pressure increased due to .
the 25 percent total bypass capacity of the Bypass Valves. The pressure, initially ~
.at 1035.psig, increased to approximately 1100 psig and resulted in the automatic actuation of the Main' Steam /Terget Rock two-stage relief valves RV-203-3A (s/n
,, 1040), RV-203-3B (s/n 104P.), and RV-203-3C (s/n 1046). Relief valve RV-203-3D (s/n <
L 1025)'did not actuate. l l
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u 3 NUCLEAR E.tivtATORY COMusseeced LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Anaovfo ove =o mo-oio.
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s EXPinf 8: l'31/W F AC4LITY 884488 tu DOCKli NUllSER 83) Llh NUMDIR tel PA06 t3l Pilgrim Nuclear Power Station "'" '
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As expected, the RV water level decreased in response to the scram because of ',
-shrink-(i.e., decrease in the void fraction in the RV"wr.ter). The RV water level eventually decreased to approximately -10 inches (narrow range level).. The decrease in RV water level, to less than the low RV water level setpoint '
(calibrated att approximately +12 inches) resulted in automatic actuations of the Primary Containment Isolation Control System (PCIf,) and Reactor Building Isolation Control System (RBIS).
The PCIS actuation resulted in the following lesigned responses:
(PCS)/ Reactor Hater Sample isolation valves A0-220-44'and -45.
- Automatic closing.of'the inboard and outboard PCS' Group 2 (two) isolation valves that were open. _g
- The PCS Group 3 (three)/ Residual Heat Removal System . isolation valves, iin' the , '
closed position,: remained closed. ' 1 e- Automatic. closing of the inboard and outboard PCS Group 6 (six)/ Reactor Hater 4
- Cleanup (RHCU) System isolation valves and a temporary interruption in RHCU System operation, i m The RBIS actuation resulted in the automatic closing of the Reactor i Building / Secondary Containment System (SCS) supply and-exhaust ventilation dampers.
~(Trains. 'A' and ~ 'B'), and the automatic start of Trains 'A' and 'B' of the
.SCS/ Standby Gas-Treatment System (SGTS).
? Initial Control Room operator response was orderly and included the.following. The-reactor mode selector switch'was-moved from the RUN position to the REFUEL position
- and the ' reactor. feedpumps were' tripped in accordance with procedure 2.1.6, " Reactor Scram"'.-Emergency Operating Procedure (E0P)-01, "RPV Control", was.. initiated when the:RV water: level decreased to less than +9 inches (narrow' range) and was terminated when the RV water level increased to greater'than +9 inches. Meanwhile, .
the High Pressure Coolant Injection System (HPCIS) was manually started in the full-flow test mode as.a. precautionary pressure control measure'and in accordance with n the guidance provided in E0P-01. The Residual Heat Removal System (RHRS) loop 'A' l< (pump 'A'),was placed in the Suppression Pool Cooling (SPC) mode in accordance with.
procedure 2.2.86, " Residual Heat Removal", because of the heat addition from the steam discharged into the Suppression Pool via the discharge piping from the-relief valvesiand HPCIS turbine. The Suppression Pool temperature was logged in '
+
accordance with procedure 2.1.19, " Suppression Chamber Temperatures". Procedures 2.1.5. Attachment 1, " Shutdown /Cooldown Checklist", and 2.1.7 Attachment 1, "RPV Temperature'and Pressure Checklist", were initiated. The PCIS circuitry was reset L1 and the RHCU System was returned to service. The RBIS circuitry was reset, the
'SGTS was returned to normal standby service and the Reactor Building ventilation system was returned to normal service.
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UCENSEE EVENT REPORT (LER) TEXT CONTINUATION - - maovio ove no mo-m4 ii g *
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(.,, 9.C4LITY NAME (1) DOCKET fdUMBER (U LIR NUMetR (6) PA08 (3) ~
Pilgrim Nuclear P e r Station " ' "
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gl 0 ' Ol 4 oF Ol8 7 Iw a ., . o .~ - m w., use,wn L/ The NRC Operations-Center was notified of the event in accordance with-10 CFR 50.72 b on May 13,.1990 at.1734 hours0.0201 days <br />0.482 hours <br />0.00287 weeks <br />6.59787e-4 months <br />. Failure and Malfunction Report 90-159 was written to document the event. A post trip review of the eventwas performed in accordance with procedure 1.3.37, " Post Trip Reviews".
BACKGROUND i
Prior to'the event, steady state operating conditions existed and included.the '
F following. The RV water level was +29 inches (narrow range) and the Feedwater E System was being controlled in the automatic three element control mode. The RV i -pressure .was 1035 psig and was being controlled via the Electric Pressure <
-Regulator. The Turbine speed was approximately 1800 rpm and Turbine first stage ,
pressure was approximately 730 psig. The Recirculation System pumps were being controlled in the local-manual control mode. The Condensate System and'Feedwater System pumps were-all in service. Except for Bus A6, the APDS was energized by-the
.UAT. The preferred source of offsite power, 345 KV transmission lines 342 and 355, were in service. The 345 KV switchyard air circuit breakers ACB-102 (352-2),
JACB-103'(352-3), AC8-104 (352-4), and ACB-105 (352-5) were in service. T,te 23 KV ,
backup ~ source of offsite power was in service. Thunderstorm activity wa*, reported i f in the' region, j
Just prior to the event on May 13 1990 at 1603 hcurs,~ numerous Main Control Room
. alarms ' occurred in a short interval of time and included Panel C-3R, " Unit #1 Generator: Low Excitation"..and " Unit #1 Generatot nelay Trip". After the event,.
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the regional power agency (REMVEC) reported thir the Pilgrim Station; trip occurred-at the same time that'a 345 KV transmission _ syn .m line (322) fault occurred.
Transmission line 322 is related to the nearby. canal Station and, via transmission, line' 342, to Pilgrim ~ Station. A static wire (lightning' protection) for line 322 3 fell onto its-conductors and caused a fault. The fault.resulted in,an electrical
' disturbance that was detected and isolated by protective devices on line 322. The
%.' momentary disturbance was sensed by the transmissi.on system prior to the isolation L
offline 322. .The disturbance did not result in a trip of the Canal Station i
. generators but did result in the trip of Pilgrim Station, t g The cause for the Pilgrim Station trip was the momentary fault on line 322 (transmitted via line 342)'and the absence of the telephone relay time delay ('X'
, coll) function' of-the loss-of-field relay (240) at(Pilgrim Station. The
- disturbance actuated the impedance (Z) and directional (D) and voltage (V) units of
, *. .the relay.(240) that is part of the Generator's protective circuitry. -.The .'X' coi?
is' normally energized and is designed to change state (drop.out) 15 cycles (i.e.,
0.25 second) after it de-energizes due to a disturbance (Z and D and V). The time delay is provided to prevent a-trip of the Generator due to a momentary fault on ,
the 345'KV transmission system. The failure of the 'X' coil resulted in.no time delay for relay 240 and consequently, the Pilgrim Station Generator Lockout Relay ;
(286-1) actuated at the time of the momentary fault. The loss-of-field relay (240) was manufactured by Hestinghouse Electric Corporation, type KLF-1, style 2928333A10, 125 VDC, 5 Amps, 69 volts, 60 Hertz.
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9dCILITY fsAf tt (H DOC 8LET NUMBER Gl LE R NUMSER (61 PA04 (31 Pilgrim Nuclear Power Station " ' "
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olo ol 5 0F 0 l8 The non safety-related loss-of-field relay (240) is functionally tested in accordance with procedure 3.M.3-39 Attachment 1 "Tufbine/ Generator Lockout Test and Associated Annunciator Verification" and calibrated in accordance with j Attachment 2 " Calibration of Turbine / Generator Relays". The functional test includes a check (operation) of the relay's alarm functions and trip functions, i The relay was most recently functionally tested and calibrated with satisfactory '
.results while shutdown on October 26, 1989. The operation of the telephone relay-was tested in accordance with the vendor manual (V-0250) that does not include or specify a calibration (timing) of the relay's inherent time delay. The time delay ;
of the relay was built-in and not adjustable, and therefore was not checked as part !
of the calibration. The relay (240) was installed during original plant I construction (c. 1972). A search of the Nuclear Plant Reliability Data System (NPRDS) revealed no other failures of a KLF-1 relay. Therefore, the cause for the open ('X') coil of the telephone relay is believed to be random or. age related failure.. The cause for the open coil is being investigated'and an update to this t report will be submitted if the investigation reveals significant newlinformation. !
l CORRECTIVE ACTION The unit returned to commercial service on May 15, 1990 at 1030 hours0.0119 days <br />0.286 hours <br />0.0017 weeks <br />3.91915e-4 months <br />.
The loss-of-field relay (240) was replaced on May 16, 1990 with another relay (KLF-1) having an adjustable time delay. Interim measures taken until the relay-was replaced consisted of modifying the relay via a Temporary Modification (TM 90-11) that was supported by a Safety Evaluation (SE 2470). Essentially,'the relay's-(240) trip function was disabled without affecting the relay's alarm functions.
The relay's.(240) calibration sheet has been revised to include a calibration of the new' relay's adjustable time delay. The loss-of-field relay (240) is the only.
.one of'its- type (KLF-1) installed at Pilgrim Station.
An Engineering Service Request (ESR 90-327) has been written to determine if any other relay (s), included in procedure 3.M.3-39 or 3.M.3-40 (Relay House Testing),
is equipped with a built-in ' time delay that may need additional testing.
SAFETY CONSEOUENCES This event. posed no threat to the public health and safety.
The Technical Specification 2.2.B limiting safety system setting for the Main Steam System / Pressure Relief System (PRS) relief valves is 1095 to 1115 psig with a tolerance of +/- 11 psi. The setpoint of the relief valves is 1115 psig.
Therefore, the setpoint range of the relief valves including tolerance is 1104 psig to 1126 psig. During the event, the highest RV/ Main Steam System pressure that occurred was approximately 1100 psig. The two-stage Target Rock relief valves (RV-203-3A/3B/3C/30) are installed in Main Steam pipelines 'A' (RV-203-3A and -3D) and 'O' (RV-203-3B and -3C).
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increased rapidly (i.e., 38 psig in 0.5 second) until RV-203-3A (s/n 1040).and RV-203-3B (s/n 1048) actuated. After RV-203-3A and -3B actuated, the pressure continued to increase, but in a,less rapid manner, for another 0.5 second until RV-203-3C (s/n 1046) actuated. -After RV-203-3C actuated, and with RV-203-3A and
-3B still actuated, pressure remained relatively constant for another 1.2 seconds and RV-203-3C then closed. After RV-203-3C closed, and with RV-203-3A and -3B-still actuated, pressure decreased (i.e., 30 psig in 2 secondt) and RV-203-3A and n-3B then closed. The duration of the pressure transient, fron initial to maximum to initial (all relief valves closed), was approximately 5 (five) seconds. Relief valve RV-203-30 (s/n 1025) did not actuate for the pressure relief function. The t relief valve (s/n-1025) was.most recently tested at an offsite t u t facility on August 2,1988 with certified as-left popping pressures of 1114 ps!g +/- 1 (one) psig. The load rejection with. bypass experienced during this event is bounded by the transient analysis described in the Updated Final Safety Analysis Report section 14.4.3, " Generator Load Rejection Hithout Bypass". The actuation (opening) of some or all of the _4 (four) two-stage relief valves (RV-203-3A/3B/3C/30) is an expected response to a load rejection with bypass at 100 percent power.
The. Technical Specification 2.2.C limiting safety system setting for the Main Steam / PRS safety valves (RV-203-4A and -48) is 1240 +/- 13 psi. . During the event, the' highest RV' pressure that occurred (1100 psig) was approximately 140 psig less than the. safety valves' setpoint (1240 psig).
The HPCIS was . manually started in the full flow test code in accordance with procedure 2.2.21 [HPCIS] section 7.4.2'and in accordance with the guidance of "
- E0P-01. In the full flow test mode, steam from Main Steam pipeline 'D' is supplied to the HPCIS turbine and is exhausted to the Suppression Pool, and water from the ,
Condensate Storage Tanks (CST) is supplied to the HPCIS pump and is returned to the CST via'.the. test return line. The injection function of the HPCIS was not used.
- The scram signal was the designed response to the Turbine Control Valves Fast Closure (i.e., opening of PS-37/38/39/40). The closure was the expected designed
- response to a load -rejection with the Turbine first stage pressure at approximately 730 psig, i.e. greater'than the scram bypass setpoint (calibrated at 108 psig +/- 3 psig)Lcorresponding to 25 percent of the normal first' stage pressure).
The decrease in the RV water level was the expected response to the scram and accompanying shrink in the RV water. The PCIS and RBIS actuations were the expected-designed responses to a low RV water level condition, i.e. +12 inches (narrow range).
The Technical Specification 2.1.I limiting safety system setting for actuation of the Core Standby Cooling Systems (CSCS) is -49 inches. During the event, the lowest RV water level that occurred (-10 inches) was approximately 36 inches above the CSCS setpoint (calibrated at approximately -46 inches). In addition, the level
(-10 inches) was approximately 117.5 inches above the level that corresponds to the top of the active fuel zone (-127.5 inches).
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[& 1 This report'is submitted in_accordance with 10 CFR 50.73 (a)(2)(iv) because the kPS l d<i 3 .y <
was actuated.
H k SIMILARITY TO PREVIOUS EVENTS 1
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'{ - A review was conducted of Pilgrim Station Licensee Event Reports. (LERs) submitted 1 since January 1984. The review focused on LERs submitted in accordance with l' 10 CFR 50.73(a)(2)(iv) that involved the loss-of-field relay, a load rejection or i similar scram. The review identified similar events reported in LERs- l I 50-293/85-025-00 and 89-026-00.
For LER 85-025-00, an automatic scram occurred on September 1,1985 at 0521 hours0.00603 days <br />0.145 hours <br />8.614418e-4 weeks <br />1.982405e-4 months <br />
+ Lwhile at 32 percent reactor power. At the time of the event, the Main. Condenser twas being backwashed and a live washdown of the 345 KV switchyard insulators was being performed to reduce arcir;g due to salt from a heavy ocean storm. A 345 KV phase.'B' insulator, located on the Main Transformer side of the switchyard ACB-104, disintegrated:and resulted in a load rejection. The cause for the scram was high RV pressure that resulted from the load rejection.- The cause for the
~
event was due to thesforces of nature (i.e. high winds'and salt air). Please note 1 that the event occurred while at 32' percent reactor power. At-that power level, Lthe~ Turbine first stage pressure was approximately-200 psig. An RPS scram signal due to a Turbine Control-Valves Fast Closure (i.e., PS-37/38/39/40) or Turbine Stop l Valves. closure (i.e., less than 90 percent open) would have occurred if the Turbine. ,'
first-stage pressure was greater than approximately 280 psig (i.e., scram bypass setpoint for 45. percent of ~the normal first stage pressure). The scram bypass setpoint was changed from 280 psig to 108 psig (+/- 3 psig) via a modification
. (PDC 87-48) during Refueling Outage number 7.
For LER 89-026-00,- an automatic .RPS scram signal and . scram occui red. on -
August-30,_1989_at 1917-hours.while at 65 percent reactor. power. _The cause for_the ,
scram signal was'high RV pressure (ultimately 1069 psig) that occurred as a result of an automatic Turbine: runback. The runback included the automatic adjustment of the Turbine Control Valves and sequential opening of'the Turbine Bypass Valves.
The runback occurred as a result of the failure of the primary winding of the Main
+
Generator'24 KV phase "A' potential transformer and a Generator-Voltage Balance-Relay (260) wiring' error that:affected the transfer function'of the Generator's Voltage.Regelator. The wiring error was due to a drawing error. 'The error was not prev nusly detected because the surveillance test procedure (3.M.3-39) used to ifunctionaily. test the relay (260), although demonstrating the voltage balance relay
" function and alarm functions, did not include a step (s) to identify the auxiliary T ; relay U.60X1 or 260X2) that actuates the same alarm (Panel C-3R, " Generator
. Potential Fuse Blown") during the test (s).
NRC FORM 34GA -
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., .OCENSEE EVEN'T REPORT (LER) TEXT CONTINUATION maovio ove no aisoaion
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ENERGY INDUSTRY IDENTIFICATION SYSTEM (EIIS) CODES:
The EIIS codes for this report are as follows:- ,
COMPONENTS CODES Relay, Voltage and Power Directional (240)- 92 ;
Valve, Relief' RV y ,
SYSTEMS Containment Isolation Control System (PCISsRBIS) JH
= Engineered Safety Features-Actuation System JE (PCIS, RBIS, RPS)~
Hain Generator Output System EL Main' Steam System SB Hain Turbine System TA
- Plant Protection; System (PRS) JC !
1: _ Reactor Hater Cleanup (RWCU) System CE- !
- Standby Gas-Treatment System (SGTS) 'BH-Switchyard System (345 KV)- 'FK-
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'. NRC FORM 366A
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