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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046C3131993-07-28028 July 1993 LER 93-015-00:on 930630,HPCI Sys Declared Inoperable Due to Indicated Flow During Surveillance.Caused by Foreign Matl That Plugged Portion of Restricting Orifice.Restricting Orifice Removed,Cleaned & reinstalled.W/930728 Ltr ML20046B5241993-07-26026 July 1993 LER 93-007-01:on 930317,automatic Closing of RCIC Sys Turbine Steam Supply Isolation Valves Occurred Due to High Steam Flow Signal.Increased Frequency of Valve Testing from Monthly to weekly.W/930726 Ltr ML20045F8601993-06-30030 June 1993 LER 93-014-00:on 930531,automatic Scram Occurred,Resulting from Operation of Auxiliary Transformer Differential Relay During Power Ascension.Uat Phase B & C Differential Relays Left Interchanged as Investigative aid.W/930630 Ltr ML20045E2301993-06-25025 June 1993 LER 93-013-00:on 930530,RCIC Sys Declared Inoperable & 7 Day TS 3.5.D.2 LCO Entered Due to Speed Oscillations Which Occurred After Several Minutes of steady-state Operation. Caused by Actuator Failure.Actuator replaced.W/930625 Ltr ML20045E2251993-06-25025 June 1993 LER 93-012-00:on 930529,unplanned PCIS Group I Isolation Signal Occurred While Opening MSIV During Startup,Resulting in Automatic Closing of Related Valves.Caused by Licensed Operator Error.Group 1 Isolation reset.W/930625 Ltr ML20045D6941993-06-23023 June 1993 LER 93-011-00:on 930525,determined That Initial as-found Popping Pressures of Pilot Valves for Three Target Rock Main Steam Relief Valves Out of TS Tolerance.Caused by Setpoint Drift.Valves Reworked & Reassembled by Target Rock Corp ML20045D1861993-06-18018 June 1993 LER 93-010-00:on 930519,SUT Became de-energized During Planned Calibr of Turbine/Generator Relays Lockout Test While Shut Down.Caused by Personnel Error.Discussion Conducted W/Personnel Re Attention to detail.W/930618 Ltr ML20044H0441993-06-0202 June 1993 LER 93-009-00:on 930504,circuit Breaker Did Not Close During Planned Bus Transfer Due to Loose Control Circuit Wire.Lug Replaced & Reterminated on 930505 & Post Work Testing Completed W/Satisfactory results.W/930602 Ltr ML20024G7451991-04-24024 April 1991 LER 91-005-00:on 910325,diesel Generator Inoperable,Causing Loss of Ac Power to Train B Components of Safety Sys & Actuating Portions of Primary/Secondary Containment Sys. Caused by Voltage Regulator failure.W/910424 Ltr ML20029A6721991-02-25025 February 1991 LER 91-001-00:on 910125,automatic Primary Containment Isolation Control Sys Group 5 Actuation Occurred,Resulting in Closing of RCIC Turbine Steam Supply Isolation Valves. Caused by High Flow conditions.W/910225 Ltr ML20028G9731990-09-20020 September 1990 LER 89-036-01:on 891122,determined That HPCI Sys Inoperable Due to Inoperable Gland Seal Condenser Blower Motor.Caused by age-related Wear of Motor.Blower Motor Replaced & Blower Tested W/Satisfactory results.W/900920 Ltr ML20028G9121990-09-18018 September 1990 LER 89-037-01:on 891130,primary Containment/Traversing in-core Probe Ball Valve Discovered to Be Almost Full Open. Caused by Damage to Valve Stem Due to Manual Manipulation of Stem.Ball Valve & Solenoid Actuator replaced.W/900918 Ltr ML20043G3541990-06-12012 June 1990 LER 90-008-00:on 900513,automatic Scram Resulting from Load Rejection Occurred While at Full Power,Resulting in Trip of Generator Field Breakers.Caused by Fault on Offsite 345 Kv Transmission sys.Loss-of-field Relay replaced.W/900612 Ltr ML20043F8291990-06-0606 June 1990 LER 90-007-00:on 900507,discovered That Drywell to Suppression Chamber Vacuum Breaker Surveillance Not Performed Prior to Startup in 1988.Caused by Misunderstanding of requirements.W/900606 Ltr ML20042F5911990-04-30030 April 1990 LER 90-006-00:on 900330,determined That Position of Primary Containment Sys Isolation Valve Not Recorded Daily,Per Tech Specs.Review Performed to Determine If Other Problems Existed.Plant Shut Down & Review performed.W/900430 Ltr ML20012F5751990-04-0606 April 1990 LER 90-003-00:on 900311,automatic Actuation of Main Steam Sys Group 1 Portion of Primary Containment Isolation Control Sys Occurred.Caused by False High Reactor Vessel Water Level Signal.Procedure Developed Re backfill.W/900406 Ltr ML20012E9831990-03-30030 March 1990 LER 90-002-00:on 900228,determined That Max Fraction of Limiting Power Density Not Checked Daily During Reactor Power Operation,Per Tech Spec 4.1.B.On 900323,addl Tech Spec Issue Discovered.Tech Specs changed.W/900330 Ltr ML20012C4871990-03-12012 March 1990 LER 90-001-00:on 900209,24 H Limiting Condition for Operation Entered When Two RCS Instrumentation Excess Flow Check Valves Inappropriately Verified Operable During Testing.Cause Undetermined.Two Valves replaced.W/900312 Ltr ML20005G0981990-01-0808 January 1990 LER 89-038-00:on 891208,unplanned Automatic Reactor Protection Sys Scram Signal & Reactor Scram Occurred.Caused by False Low Reactor Vessel Water Level Signal.Local Level Indicators Satisfactorily calibr.W/900108 Ltr ML20005F8481990-01-0808 January 1990 LER 89-039-00:on 891209,automatic Actuation of RHR Sys Portion of Primary Containment Isolation Control Sys Occurred.Caused by Hydrodynamic Transient That Actuated Protective High Pressure switches.W/900108 Ltr ML20005E8551989-12-30030 December 1989 LER 89-037-00:on 891130,discovered That Traversing in-core Probe Ball Valve,Mfg by Consolidated Controls,Inc,Closed,In Violation of Tech Specs.Caused by Damage to Valve Stem.Ball Valve & Actuator replaced.W/891230 Ltr ML20011D1361989-12-11011 December 1989 LER 89-035-00:on 891111,inadvertent Actuation of Portion of Secondary Containment Sys During Surveillance Testing Occurred.Caused by Location of Radiation Isolation Control Sys Channel a Logic Relay.Procedure revised.W/891211 Ltr ML20005D7421989-12-0606 December 1989 LER 89-033-00:on 891106,automatic Actuation of Group 1 Portion of Primary Containment Isolation Control Sys (PCIS) Occurred.Caused by High Reactor Vessel Water Level.Manual Valve Closed & PCIS Logic Circuitry reset.W/891206 Ltr ML19351A4581989-12-0606 December 1989 LER 89-034-00:on 891108,determined That Reactor Pressure Exceeded 150 Psig on 891107 W/O Performing Surveillance Procedure 8.5.4.4, HPCI Valve Operability Test. Caused by Personnel Error.Procedure initiated.W/891206 Ltr ML19332D1421989-11-22022 November 1989 LER 89-031-00:on 891024,closing Times for Two in-series Primary Containment Isolation Valves Exceeded Acceptance Criteria During Shutdown Testing.Cause Undetermined.Closing Time Retested W/Satisfactory results.W/891122 Ltr ML19332D6231989-11-20020 November 1989 LER 89-032-00:on 891020,pneumatic Pressure Drop for Two of Four Automatic Depressurization Sys Accumulators Discovered Greater than Max Acceptable Value.Caused by Leakage from Seat of Supply Check Valves.Seat replaced.W/891120 Ltr ML19324C3181989-11-0909 November 1989 LER 88-002-01:on 880117,full Reactor Protection Sys Scram Trip Signal Occurred During Surveillance Test,Resulting in Incomplete Actuations.Caused by Procedure Inadequacy.Logic Relay Replaced & Procedure revised.W/891109 Ltr ML19324B1131989-10-21021 October 1989 LER 89-030-00:on 890926,control Room High Efficiency Air Filtration Sys Flowrate non-conservative Due to Procedure Error.Caused by Transcription Error.Procedure Revised & Test Reperformed Using Corrected procedure.W/891021 Ltr ML19325D4681989-10-16016 October 1989 LER 89-029-00:on 890914,locked High Radiation Area Door Found to Have Been Unsecured Contrary to Tech Spec 6.13.2. Caused by Failure to Adhere to Approved Procedures. Training on Access Requirements initiated.W/891016 Ltr ML19325D1861989-10-10010 October 1989 LER 89-028-00:on 890907,HPCI Sys Declared Inoperable Because Mechanical Overspeed Trip Occurred During Surveillance Test. Caused by Failure of Ramp Generator Signal Converter Module. Module Removed & Sent to Mfg for exam.W/891010 Ltr ML17277B8221984-07-20020 July 1984 LER 82-049/01X-1:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting.Caused by Personnel Error.Valve Removed & Replaced W/Properly Set Spare Valve. Procedure revised.W/840720 Ltr ML20024C3231983-06-24024 June 1983 Updated LER 82-038/03X-1:on 820817,RCIC Steam Line High Differential Pressure Alarm Received.Caused by Air in Sensing Lines to Pressure Switches.Cross Threaded Cap Found on in-line Snubber.Snubber replaced.W/830624 Ltr ML20024C2211983-06-24024 June 1983 Updated LER 80-053/03X-1:on 800814,0907 & 14,HPCI Turbine Exhaust Line Snubber 23-3-36 Determined Inoperable.Caused by Transient Hydrodynamic Shock During Startup & Shutdown. Snubbers upgraded.W/830624 Ltr ML20024B8451983-06-24024 June 1983 LER 83-031/03L-0:on 830528,HPCI Sys Made Inoperable to Repair Steam Leak on AO 2301-31.Caused by Leaking Stem Packing.Packing Replaced.Valve Tested Satisfactorily.Sys Returned to svc.W/830624 Ltr ML20024B8321983-06-24024 June 1983 LER 83-030/03L-0:on 830527,both HPCI Area Smoke Detection Sys Alarmed in Main Control Room.Caused by Valve A02301-31 Steam Leak Causing False Indications.Valve repaired.W/830624 Ltr ML20024C3101983-06-21021 June 1983 Updated LER 79-007/03X-1:on 790212,while Performing Test 8.7.4.3,valves AO-5033A,CV-5065-10,15,16 & 17 Failed to Give Proper Position Indication When Cycled & to Close within Specified Tolerance.Cause Not stated.W/830621 Ltr ML20024A8861983-06-16016 June 1983 LER 83-027/03L-0:on 830518,during Routine Insp,Folding Fire Door Found Inoperable.Caused by Operating Cable Becoming Detached from Pulley Due to Slack.Cable Reattached & Operating Mechanism adjusted.W/830616 Ltr ML20023D1691983-05-0909 May 1983 Updated LER 82-008/01X-1:on 820331,HPCI Injection Valve MO-2301-8 Failed to Open in Required Manner.Caused by Missing Wire Jumper Intended to Bypass Motor Operator Torque Switch.Jumper Installed & Valve Tested Satisfactorily ML20023D0671983-05-0909 May 1983 LER 83-021/03L-0:on 830411,during Surveillance Test 8.7.4.3, Primary Containment Isolation Valve AO-5033B Failed to Meet 10-s Closing Time Requirements.Caused by Lubricant Infiltrating Solenoid Valve Components.Components Replaced ML20023D0181983-05-0404 May 1983 LER 83-022/03L-0:on 830413,overload on Valve Motor 1301-17 Resulted in Loss of High Pressure Core Cooling Backup Capability.Caused by Oxidation in Motor End Bell & Motor Brushes,Due to Humidity Caused by Leaking Valve Packing ML20028G1591983-01-28028 January 1983 LER 83-002/01T-0:on 830116,flow Ref off-normal Alarm Received.Average Power Range Monitor Flux Scram Trip Settings Affected.Cause Under Investigation.Flow Inputs Monitored & Amplifier B Recalibr ML20028F4121983-01-17017 January 1983 LER 83-002/01X-0:on 830116,while Clearing off-normal Alarm for Flow Comparators,Average Power Range Monitor Flux Scram Trip Settings Found in Nonconservative Direction.Caused by Drifting Proportional Amplifiers.Settings Checked Daily ML20028B0421982-11-16016 November 1982 LER 82-049/01T-0:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting of 1240 Psig, Exceeding Tech Specs.Caused by Personnel Error.Set Valve Removed,Procedure Adherence Stressed & Procedure Revised ML20027C9801982-10-20020 October 1982 LER 82-039/03L-0:on 820920,timing Tests of Three Reactor Water Cleanup Isolation Valves 1201-2,-5 & -80 Not Completed within Allowed Time.Caused by Operational Constraints Requiring Testing at Reduced Power ML20027C9941982-10-20020 October 1982 LER 82-040/03L-0:on 820920,found Reactor Protection Sys Initiation Function of Turbine Stop Valve Completed 1 Day Late.Caused by Decision to Defer Test Due to MSIV D Line Isolation.Tracking Sys Implemented to Prevent Recurrences ML20052B9141982-04-23023 April 1982 LER 82-010/03L-0:on 820326,during Review of Testing Requirements,Surveillance Test 8.I.4 Standby Liquid Control Sys Found Not Verified.Caused by Breakdown in Multidiscipline Review of Results ML20052F2071982-04-14014 April 1982 Updated LER 81-060/03X-1:on 811020,determined Potential Exists to Reduce Number of Operable APRM & IRM Instrument Channels in Rod Block Trip Sys to Below Tech Spec Min ML20050A6321982-03-19019 March 1982 Updated LER 82-055/01T-1:on 810926,during Shutdown,Yarway Level Indicators Started Oscillating.Drywell Temp Was 240 F at 81-ft W/Elevation Coolant Temp 220 F.Caused by Ineffective Drywell Cooling.Ventilation Returned to Svc ML20050A4521982-03-19019 March 1982 LER 82-006/01T-0:on 820304,while Performing Maint Re SIL 352 on Pressure Adjustment Mechanism HPCI Stop Valve,Three Broken cap-screws Found.No Cause Determined.Screws Examined, Replaced & Sys Returned to Svc ML20050A4331982-03-19019 March 1982 Updated LER 81-062/01X-1:on 811116,Wyle Labs Informed Util That Two Target Rock Safety Relief Valves Had Not Passed Setpoint Tests.Caused by Setpoint Shift Due to Changes to Designed Differential Forces from Excessive Pilot Leakage 1993-07-28
[Table view] Category:RO)
MONTHYEARML20046C3131993-07-28028 July 1993 LER 93-015-00:on 930630,HPCI Sys Declared Inoperable Due to Indicated Flow During Surveillance.Caused by Foreign Matl That Plugged Portion of Restricting Orifice.Restricting Orifice Removed,Cleaned & reinstalled.W/930728 Ltr ML20046B5241993-07-26026 July 1993 LER 93-007-01:on 930317,automatic Closing of RCIC Sys Turbine Steam Supply Isolation Valves Occurred Due to High Steam Flow Signal.Increased Frequency of Valve Testing from Monthly to weekly.W/930726 Ltr ML20045F8601993-06-30030 June 1993 LER 93-014-00:on 930531,automatic Scram Occurred,Resulting from Operation of Auxiliary Transformer Differential Relay During Power Ascension.Uat Phase B & C Differential Relays Left Interchanged as Investigative aid.W/930630 Ltr ML20045E2301993-06-25025 June 1993 LER 93-013-00:on 930530,RCIC Sys Declared Inoperable & 7 Day TS 3.5.D.2 LCO Entered Due to Speed Oscillations Which Occurred After Several Minutes of steady-state Operation. Caused by Actuator Failure.Actuator replaced.W/930625 Ltr ML20045E2251993-06-25025 June 1993 LER 93-012-00:on 930529,unplanned PCIS Group I Isolation Signal Occurred While Opening MSIV During Startup,Resulting in Automatic Closing of Related Valves.Caused by Licensed Operator Error.Group 1 Isolation reset.W/930625 Ltr ML20045D6941993-06-23023 June 1993 LER 93-011-00:on 930525,determined That Initial as-found Popping Pressures of Pilot Valves for Three Target Rock Main Steam Relief Valves Out of TS Tolerance.Caused by Setpoint Drift.Valves Reworked & Reassembled by Target Rock Corp ML20045D1861993-06-18018 June 1993 LER 93-010-00:on 930519,SUT Became de-energized During Planned Calibr of Turbine/Generator Relays Lockout Test While Shut Down.Caused by Personnel Error.Discussion Conducted W/Personnel Re Attention to detail.W/930618 Ltr ML20044H0441993-06-0202 June 1993 LER 93-009-00:on 930504,circuit Breaker Did Not Close During Planned Bus Transfer Due to Loose Control Circuit Wire.Lug Replaced & Reterminated on 930505 & Post Work Testing Completed W/Satisfactory results.W/930602 Ltr ML20024G7451991-04-24024 April 1991 LER 91-005-00:on 910325,diesel Generator Inoperable,Causing Loss of Ac Power to Train B Components of Safety Sys & Actuating Portions of Primary/Secondary Containment Sys. Caused by Voltage Regulator failure.W/910424 Ltr ML20029A6721991-02-25025 February 1991 LER 91-001-00:on 910125,automatic Primary Containment Isolation Control Sys Group 5 Actuation Occurred,Resulting in Closing of RCIC Turbine Steam Supply Isolation Valves. Caused by High Flow conditions.W/910225 Ltr ML20028G9731990-09-20020 September 1990 LER 89-036-01:on 891122,determined That HPCI Sys Inoperable Due to Inoperable Gland Seal Condenser Blower Motor.Caused by age-related Wear of Motor.Blower Motor Replaced & Blower Tested W/Satisfactory results.W/900920 Ltr ML20028G9121990-09-18018 September 1990 LER 89-037-01:on 891130,primary Containment/Traversing in-core Probe Ball Valve Discovered to Be Almost Full Open. Caused by Damage to Valve Stem Due to Manual Manipulation of Stem.Ball Valve & Solenoid Actuator replaced.W/900918 Ltr ML20043G3541990-06-12012 June 1990 LER 90-008-00:on 900513,automatic Scram Resulting from Load Rejection Occurred While at Full Power,Resulting in Trip of Generator Field Breakers.Caused by Fault on Offsite 345 Kv Transmission sys.Loss-of-field Relay replaced.W/900612 Ltr ML20043F8291990-06-0606 June 1990 LER 90-007-00:on 900507,discovered That Drywell to Suppression Chamber Vacuum Breaker Surveillance Not Performed Prior to Startup in 1988.Caused by Misunderstanding of requirements.W/900606 Ltr ML20042F5911990-04-30030 April 1990 LER 90-006-00:on 900330,determined That Position of Primary Containment Sys Isolation Valve Not Recorded Daily,Per Tech Specs.Review Performed to Determine If Other Problems Existed.Plant Shut Down & Review performed.W/900430 Ltr ML20012F5751990-04-0606 April 1990 LER 90-003-00:on 900311,automatic Actuation of Main Steam Sys Group 1 Portion of Primary Containment Isolation Control Sys Occurred.Caused by False High Reactor Vessel Water Level Signal.Procedure Developed Re backfill.W/900406 Ltr ML20012E9831990-03-30030 March 1990 LER 90-002-00:on 900228,determined That Max Fraction of Limiting Power Density Not Checked Daily During Reactor Power Operation,Per Tech Spec 4.1.B.On 900323,addl Tech Spec Issue Discovered.Tech Specs changed.W/900330 Ltr ML20012C4871990-03-12012 March 1990 LER 90-001-00:on 900209,24 H Limiting Condition for Operation Entered When Two RCS Instrumentation Excess Flow Check Valves Inappropriately Verified Operable During Testing.Cause Undetermined.Two Valves replaced.W/900312 Ltr ML20005G0981990-01-0808 January 1990 LER 89-038-00:on 891208,unplanned Automatic Reactor Protection Sys Scram Signal & Reactor Scram Occurred.Caused by False Low Reactor Vessel Water Level Signal.Local Level Indicators Satisfactorily calibr.W/900108 Ltr ML20005F8481990-01-0808 January 1990 LER 89-039-00:on 891209,automatic Actuation of RHR Sys Portion of Primary Containment Isolation Control Sys Occurred.Caused by Hydrodynamic Transient That Actuated Protective High Pressure switches.W/900108 Ltr ML20005E8551989-12-30030 December 1989 LER 89-037-00:on 891130,discovered That Traversing in-core Probe Ball Valve,Mfg by Consolidated Controls,Inc,Closed,In Violation of Tech Specs.Caused by Damage to Valve Stem.Ball Valve & Actuator replaced.W/891230 Ltr ML20011D1361989-12-11011 December 1989 LER 89-035-00:on 891111,inadvertent Actuation of Portion of Secondary Containment Sys During Surveillance Testing Occurred.Caused by Location of Radiation Isolation Control Sys Channel a Logic Relay.Procedure revised.W/891211 Ltr ML20005D7421989-12-0606 December 1989 LER 89-033-00:on 891106,automatic Actuation of Group 1 Portion of Primary Containment Isolation Control Sys (PCIS) Occurred.Caused by High Reactor Vessel Water Level.Manual Valve Closed & PCIS Logic Circuitry reset.W/891206 Ltr ML19351A4581989-12-0606 December 1989 LER 89-034-00:on 891108,determined That Reactor Pressure Exceeded 150 Psig on 891107 W/O Performing Surveillance Procedure 8.5.4.4, HPCI Valve Operability Test. Caused by Personnel Error.Procedure initiated.W/891206 Ltr ML19332D1421989-11-22022 November 1989 LER 89-031-00:on 891024,closing Times for Two in-series Primary Containment Isolation Valves Exceeded Acceptance Criteria During Shutdown Testing.Cause Undetermined.Closing Time Retested W/Satisfactory results.W/891122 Ltr ML19332D6231989-11-20020 November 1989 LER 89-032-00:on 891020,pneumatic Pressure Drop for Two of Four Automatic Depressurization Sys Accumulators Discovered Greater than Max Acceptable Value.Caused by Leakage from Seat of Supply Check Valves.Seat replaced.W/891120 Ltr ML19324C3181989-11-0909 November 1989 LER 88-002-01:on 880117,full Reactor Protection Sys Scram Trip Signal Occurred During Surveillance Test,Resulting in Incomplete Actuations.Caused by Procedure Inadequacy.Logic Relay Replaced & Procedure revised.W/891109 Ltr ML19324B1131989-10-21021 October 1989 LER 89-030-00:on 890926,control Room High Efficiency Air Filtration Sys Flowrate non-conservative Due to Procedure Error.Caused by Transcription Error.Procedure Revised & Test Reperformed Using Corrected procedure.W/891021 Ltr ML19325D4681989-10-16016 October 1989 LER 89-029-00:on 890914,locked High Radiation Area Door Found to Have Been Unsecured Contrary to Tech Spec 6.13.2. Caused by Failure to Adhere to Approved Procedures. Training on Access Requirements initiated.W/891016 Ltr ML19325D1861989-10-10010 October 1989 LER 89-028-00:on 890907,HPCI Sys Declared Inoperable Because Mechanical Overspeed Trip Occurred During Surveillance Test. Caused by Failure of Ramp Generator Signal Converter Module. Module Removed & Sent to Mfg for exam.W/891010 Ltr ML17277B8221984-07-20020 July 1984 LER 82-049/01X-1:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting.Caused by Personnel Error.Valve Removed & Replaced W/Properly Set Spare Valve. Procedure revised.W/840720 Ltr ML20024C3231983-06-24024 June 1983 Updated LER 82-038/03X-1:on 820817,RCIC Steam Line High Differential Pressure Alarm Received.Caused by Air in Sensing Lines to Pressure Switches.Cross Threaded Cap Found on in-line Snubber.Snubber replaced.W/830624 Ltr ML20024C2211983-06-24024 June 1983 Updated LER 80-053/03X-1:on 800814,0907 & 14,HPCI Turbine Exhaust Line Snubber 23-3-36 Determined Inoperable.Caused by Transient Hydrodynamic Shock During Startup & Shutdown. Snubbers upgraded.W/830624 Ltr ML20024B8451983-06-24024 June 1983 LER 83-031/03L-0:on 830528,HPCI Sys Made Inoperable to Repair Steam Leak on AO 2301-31.Caused by Leaking Stem Packing.Packing Replaced.Valve Tested Satisfactorily.Sys Returned to svc.W/830624 Ltr ML20024B8321983-06-24024 June 1983 LER 83-030/03L-0:on 830527,both HPCI Area Smoke Detection Sys Alarmed in Main Control Room.Caused by Valve A02301-31 Steam Leak Causing False Indications.Valve repaired.W/830624 Ltr ML20024C3101983-06-21021 June 1983 Updated LER 79-007/03X-1:on 790212,while Performing Test 8.7.4.3,valves AO-5033A,CV-5065-10,15,16 & 17 Failed to Give Proper Position Indication When Cycled & to Close within Specified Tolerance.Cause Not stated.W/830621 Ltr ML20024A8861983-06-16016 June 1983 LER 83-027/03L-0:on 830518,during Routine Insp,Folding Fire Door Found Inoperable.Caused by Operating Cable Becoming Detached from Pulley Due to Slack.Cable Reattached & Operating Mechanism adjusted.W/830616 Ltr ML20023D1691983-05-0909 May 1983 Updated LER 82-008/01X-1:on 820331,HPCI Injection Valve MO-2301-8 Failed to Open in Required Manner.Caused by Missing Wire Jumper Intended to Bypass Motor Operator Torque Switch.Jumper Installed & Valve Tested Satisfactorily ML20023D0671983-05-0909 May 1983 LER 83-021/03L-0:on 830411,during Surveillance Test 8.7.4.3, Primary Containment Isolation Valve AO-5033B Failed to Meet 10-s Closing Time Requirements.Caused by Lubricant Infiltrating Solenoid Valve Components.Components Replaced ML20023D0181983-05-0404 May 1983 LER 83-022/03L-0:on 830413,overload on Valve Motor 1301-17 Resulted in Loss of High Pressure Core Cooling Backup Capability.Caused by Oxidation in Motor End Bell & Motor Brushes,Due to Humidity Caused by Leaking Valve Packing ML20028G1591983-01-28028 January 1983 LER 83-002/01T-0:on 830116,flow Ref off-normal Alarm Received.Average Power Range Monitor Flux Scram Trip Settings Affected.Cause Under Investigation.Flow Inputs Monitored & Amplifier B Recalibr ML20028F4121983-01-17017 January 1983 LER 83-002/01X-0:on 830116,while Clearing off-normal Alarm for Flow Comparators,Average Power Range Monitor Flux Scram Trip Settings Found in Nonconservative Direction.Caused by Drifting Proportional Amplifiers.Settings Checked Daily ML20028B0421982-11-16016 November 1982 LER 82-049/01T-0:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting of 1240 Psig, Exceeding Tech Specs.Caused by Personnel Error.Set Valve Removed,Procedure Adherence Stressed & Procedure Revised ML20027C9801982-10-20020 October 1982 LER 82-039/03L-0:on 820920,timing Tests of Three Reactor Water Cleanup Isolation Valves 1201-2,-5 & -80 Not Completed within Allowed Time.Caused by Operational Constraints Requiring Testing at Reduced Power ML20027C9941982-10-20020 October 1982 LER 82-040/03L-0:on 820920,found Reactor Protection Sys Initiation Function of Turbine Stop Valve Completed 1 Day Late.Caused by Decision to Defer Test Due to MSIV D Line Isolation.Tracking Sys Implemented to Prevent Recurrences ML20052B9141982-04-23023 April 1982 LER 82-010/03L-0:on 820326,during Review of Testing Requirements,Surveillance Test 8.I.4 Standby Liquid Control Sys Found Not Verified.Caused by Breakdown in Multidiscipline Review of Results ML20052F2071982-04-14014 April 1982 Updated LER 81-060/03X-1:on 811020,determined Potential Exists to Reduce Number of Operable APRM & IRM Instrument Channels in Rod Block Trip Sys to Below Tech Spec Min ML20050A6321982-03-19019 March 1982 Updated LER 82-055/01T-1:on 810926,during Shutdown,Yarway Level Indicators Started Oscillating.Drywell Temp Was 240 F at 81-ft W/Elevation Coolant Temp 220 F.Caused by Ineffective Drywell Cooling.Ventilation Returned to Svc ML20050A4521982-03-19019 March 1982 LER 82-006/01T-0:on 820304,while Performing Maint Re SIL 352 on Pressure Adjustment Mechanism HPCI Stop Valve,Three Broken cap-screws Found.No Cause Determined.Screws Examined, Replaced & Sys Returned to Svc ML20050A4331982-03-19019 March 1982 Updated LER 81-062/01X-1:on 811116,Wyle Labs Informed Util That Two Target Rock Safety Relief Valves Had Not Passed Setpoint Tests.Caused by Setpoint Shift Due to Changes to Designed Differential Forces from Excessive Pilot Leakage 1993-07-28
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217E3021999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Pilgrim Nuclear Station.With ML20212C2921999-09-16016 September 1999 SER Accepting Licensee Request for Relief from ASME Code Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Pilgrim Nuclear Power Station ML20216F3511999-09-0808 September 1999 ISI Summary Rept for Refuel Outage 12 at Pnps ML20216E6881999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pilgrim Nuclear Power Station.With ML20210R3401999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Pilgrim Nuclear Power Station.With ML20209C4731999-07-0707 July 1999 Addendum to SE on Proposed Transfer of Operating License & Matls License from Boston Edison Co to Entergy Nuclear Generation Co ML20209H8251999-07-0101 July 1999 Provides Commission with Evaluation of & Recommendations for Improvement in Processes Used in Staff Review & Approval of Applications for Transfer of Operating Licenses of TMI-1 & Pilgrim Station ML20209E6191999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Pilgrim Nuclear Power Station.With ML20196H2451999-06-29029 June 1999 SER Denying Licensee Proposed Alternative in Relief Request PRR-13,rev 2.Staff Determined That Proposed Alternative Provides Insufficient Info to Determine Adequacy of Scope of Implementation ML20209A8901999-06-28028 June 1999 SER Accepting Licensee Proposed Alternative to Use Code Case N-573 for Remainder of 10-year Interval Pursuant to 10CFR50.55a(a)(3)(i) ML20209B9861999-06-23023 June 1999 Rev 13A to Pilgrim Nuclear Power Station COLR for Cycle 13 ML20217N9061999-06-21021 June 1999 Rept of Changes,Tests & Experiments for Period of 970422-990621 ML20195K3431999-06-15015 June 1999 Safety Evaluation Granting Licensee Request to Use Guidance of GL 90-05 to Repair Flaws in ASME Class 3 Salt Svc Water System Piping for Plant ML20195G8231999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Pnps.With ML20207E7471999-05-27027 May 1999 Safety Evaluation Granting Request Re Reduction of IGSCC Insp of Category D Welds Due to Implementation of HWC to License DPR-35 ML20206M1971999-05-11011 May 1999 SER Accepting Request for Approval to Repair Flaws in ASME Code Class 3 Salt Svc Water Piping at Plant ML20206J6611999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Pilgrim Nuclear Power Station.With ML20205L0221999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Pilgrim Nuclear Power Station.With ML20207J5471999-03-0909 March 1999 Training Simulator,1999 4-Yr Certification Rept ML20207F9401999-03-0101 March 1999 Long Term Program Semi-Annual Rept for Pilgrim Nuclear Power Station ML20207H5451999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Pilgrim Nuclear Power Station.With ML20196E2151998-12-31031 December 1998 1998 Annual Rept for Boston Edison & Securities & Exchange Commission Form 10-K Rept.With ML20206Q2741998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Pilgrim Nuclear Power Station.With ML20197J3591998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Pilgrim Nuclear Power Station.With ML20195C9951998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Pilgrim Nuclear Power Station.With ML20154K0721998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Pilgrim Nuclear Power Station.With ML20153D3901998-09-22022 September 1998 Safety Evaluation Granting 970707 Request to Use Guidance in GL 90-05 to Repair Flaws in ASME Class 3 Salt Svc Water Sys Piping for Pilgrim Nuclear Power Station ML20197C5011998-09-0404 September 1998 Rev 12C,Pages 4 & 5 to Pilgrim Nuclear Power Station Colr ML20197C5471998-08-31031 August 1998 Rev 12C to Pilgrim Nuclear Power Station Colr ML20151W8231998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Pilgrim Nuclear Power Station.With ML20237E2251998-08-26026 August 1998 Suppl & Revs to SE for Amend 173 for Pigrim Nuclear Power Station ML20237A9941998-07-31031 July 1998 Monthly Operating Rept for Pilgrim Nuclear Power Station ML20236U8201998-07-13013 July 1998 Rev 12B to Pilgrim Nuclear Power Station COLR (Cycle 12) ML20236P0151998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Pilgrim Nuclear Power Station ML20249A3741998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Pilgrim Nuclear Power Station.W/Undated Ltr ML20247H2081998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Pilgrim Nuclear Power Station ML20207B7601998-03-31031 March 1998 Final Rept, Pilgrim Nuclear Power Station Site-Specific Offsite Radiological Emergency Preparedenss Prompt Alert & Notification System Quality Assurance Verification, Prepared for FEMA ML20216G3911998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Pilgrim Nuclear Power Station ML20216J3741998-03-19019 March 1998 Safety Evaluation Accepting Licensee Request to Evaluate Elevated Tailpipe Temp on Safety Relief Valve SRV 203-3B ML20248L2241998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Pilgrim Nuclear Station ML20202G5251998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Pilgrim Nuclear Power Station ML20236M8511997-12-31031 December 1997 1997 Annual Rept for Boston Edison & Securities & Exchange Commission Form 10-K Rept ML20198L7701997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Pilgrim Nuclear Power Station ML20203D6101997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Pilgrim Nuclear Power Station ML20202D5761997-11-0808 November 1997 1997 Evaluated Exercise BECO-LTR-97-111, Monthly Operating Rept for Oct 1997 for Pilgrim Nuclear Power Station1997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Pilgrim Nuclear Power Station ML20217D6431997-10-0101 October 1997 Safety Evaluation Granting Request for Approval to Repair Flaws in Accordance W/Gl 90-05 for ASME Class 3 SSW Piping for Pilgrim ML20217H5621997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Pilgrim Nuclear Power Station ML20216J4131997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Pilgrim Nuclear Power Station ML20210J3321997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Pilgrim Nuclear Power Station 1999-09-08
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/, *A 8 10 CFR 50.73 BOSTON EDISON Pilgrim Nuclear Power Station Rocky Hil! Road Plymouth, Massachusetts 02360 E. T. Boulette, PhD senior Vice President-Nuclear
,r June 2, 1993 BEco Ltr.93-071 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C. 20555 Docket No. 50-293 License No. DPR-35 The enclosed Licensee Event Report (LER) 93-009-00, " Circuit Breaker Did Not Close During Planned Bus Transfer due to Loose Control Circuit Wire", is submitted in accordance with 10 CFR Part 50.73.
Please do not hesitate to contact me if there are any questions regarding this report.
O LLN C E. T. Boulette DWE/bal Enclosuro: LER 93-009-00 cc: Mr. Thomas T. Martin Regional Administrator, Region I U.S. Nuclear Regulatory Commission 475 Allendale Rd. ,
King of Prussia, PA 19406 Mr. R. B. Eaton Div. of Reactor Projects I/II !
Office of NRR - USNRC ;
One White Flint North - Mail Stop 14D1 !
11555 Rockville Pike Rockville, MD 20852 i
Sr. NRC Resident Inspector - Pilgrim Station l Standard BEco LER Distribution i
9306070$80935602 // I PDR ADOCK 05000293 /. i S PDR // I '
I NRC FORM,366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 (5-921 EXPIRES 5/31/95 EST: MATED BURDEN PER RESPONSE TO COMPT.Y W!TH THIS LICENSEE EVENT REPORT (LER) l"Su"#5b'n%"J%*0Jf0 T%rs%^2 AND RECORDS MANAGEMENT BRANCH (MNB8 7714), U.S. NUCLEAR FIEGULATORY COMMISSION, WASHINGTON, DC 20S55-0001, AND TO THE PAPERWORK REDUCTON PROJECT (3150-0104), OFFICE (See severse tof number of digfts/chareders for each W.u) OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20501 FACILITY NAME (1) DOCKET NUMBER (2) PAGE (3)
PILGRIM NUCLEAR POWER STATION 05000 - 293 1 of 8 TITLE (4)
Circuit Breaker Did Not Close During Planned Bus Transfer due to Loose Control Circuit Wire EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
SEQUENTIAL REVISION FACluTY NAME DOCKET NUMBER
.' MONTH DAV YEAR YEAR NUMBER NUMBER MONTH DAV YEAR N/A 05000 F ACluTY NAME DOCKET NUMBER 05 04 93 93 009 00 06 02 93 N/A 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 6: (Check one or more)(11)
OI 20.402(b) 20.405(c) 50.73(a)(2)(iv) 73 71(b) 000 20.405(aH1W 50mW SoMaH2W 73 M e)
LEvE 10)
_ 20.405(aH1)0i) 50.36(c)(2) X 50.73(a)(2)(vii) (D) OTHER 20.405(a)(1)(iii) 50.73(a)(2)(i) 50.73(a)(2)(viii)(A) 20.405(a)(1)(iv) 50.73fa)(210i) 50.73(a)(2)(viii)(B) Ac 20.405ta)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x) Form 3f4A)
LICENSEE CONTACT FOR THIS LER (12)
NAME TD.EPHONE NUMBER (Include Area Codel Douglas W. Ellis - Senior Compliance Engineer (508) 747-8160 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFACTURER S CAUSE SYSTE'M COMPONENT MANUFACTURER S X EC 52 G080 Y SUPPLEMENTAL REPORT EXPECTED (14) " "
EXPECTED YES NO SUBMISSION (tf yes, comp 6m EXPECTED SUBMIS3ON DATE) x DATE (15)
ABSTRACT On May 4, 1993, at 0230 hours0.00266 days <br />0.0639 hours <br />3.80291e-4 weeks <br />8.7515e-5 months <br />, a safety-related 480 VAC load center bus that is part of a safety-related bus transfer scheme became de-energized during a planned bus transfer conducted while shut down. The related motor control centers became de-energized including the motor control center of the valves that are part of the Residual Heat Removal (RHR) System / Low Pressure Coolant Injection (LPCI) function. At the time of the event, the RHR/LPCI function was not required to be operable. The bus was re-energized at 0235 hours0.00272 days <br />0.0653 hours <br />3.885582e-4 weeks <br />8.94175e-5 months <br />.
The cause of the bus and related components becoming de-energized was circuit breaker 52-102, that is part of the transfer scheme, not closing during the transfer. The cause of breaker 52-102 not closing was a loose wire-to-lug connection in the automatic transfer portion of the circuitry that controls the breaker. Corrective action taken included replacement of the lug. The bus transfer function was subsequently tested with satisfactory results.
The event occurred while shut down in a refueling outage. The Reactor Vessel (RV) head was not installed. The reactor mode selector switch was in the REFUEL position. There was no movement of a fuel assembly or fuel cask at the time of the event. This report is submitted in accordance with 10 CFR 50.73(a)(2)(vii)(D). This event posed no threat to the public health and safety.
NHC F ORM :p%A @92;
NRO FORM 366A U.S. NUCLEAR REGULATORY COMMisslON APPRoVEo BY OMB NO. 3150-0104 u-9 n , EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS LICENSEE EVENT REPORT (LER) LTZEG'"JSERIMCJkZ*,~FOT2 TEXT CONTINUATION #$UEOYRCCESSEN R NGTON 5 A TO THE PAPERWORK REDUCTION PRC11ECT (315CHn04), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR R NM PILGRIM NUCLEAR POWER STATION 05000-293 93 009 00 TEXT (if more space is required, use additional copies of NRC Form 366A)(17)
BACKGROUND Safety-related load center Bus B6 is a 480 VAC swing type bus that can be powered by Bus B1 or B2. Bus B1 is the normal power source for Bus B6 with breakers52-102 and 52-601 in the CLOSED position and with breakers52-202 and 52-602 in the OPEN position. Circuit breakers 52-102/52-202 and 52-601/52-602 are interlocked to preclude Bus B6 from being simultaneously powered by Bus B1 and Bus 82. The interlocks of breakers 52-102/52-202 are independent of the interlocks of breakers 52-601/52-602. Located at the end of this report is a figure depicting a simplified single line diagram of the emergency service portion of the Auxiliary Power Distribution System including the Bus B6 transfer breakers.
The Bus B6 automatic transfer scheme is as follows:
- If Bus B1 was powering Bus B6 and Bus B1 were to experience a loss of voltage for approximately one second and sufficient Bus B2 voltage is available, breaker 52-102 opens and 52-202 closes, and 52-601 opens and 52-602 closes.
Bus B6 would then be energized from Bus B2.
- If Bus 82 was powering Bus B6 and Bus B2 were to experience a loss of voltage for approximately one second and sufficient Bus B1 voltage is available, breaker 52-202 opens and 52-102 closes, and 52-602 opens and 52-601 closes.
Bus B6 would then be energized from Bus Bl.
- If both Bus 81 and Bus 82 were to experience a loss of voltage for approximately one second, the two breakers in the CLOSED position would open and all four transfer breakers would then be in the OPEN position. Depending upon which Bus (B1 or B2) subsequently becomes energized, the related breakers would close and Bus B6 would then be energized.
The source of control power for the four Bus B6 transfer circuit breakers is via 125 VDC Bus D6 that is supplied from 125 VDC Bus D16 or Bus D17 through an automatic transfer switch (Y10). This configuration makes the control power for the circuit breakers highly reliable and independent of the 480 VAC buses. ,
1 SYSTEMS CONFIGURATIONS PRIOR TO THE EVENT Just prior to the event, the following systems configurations existed:
- The reactor mode selector switch was in the REFUEL position. Some fuel assemblies were not installed in the core. The control rods were fully '
inserted for the core locations where fuel was installed. The Reactor Vessel (RV) water temperature was approximately 75 degrees Fahrenheit. There was no movement of a fuel cask or irradiated fuel.
NRC roRu aosA <5 ea
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 n-m EXPIRES 5/31/95 ESTlMATED BURDEN PER RESPONSE TO COMPLY WITH THIS LICENSEE EVENT REPORT (LER) 10^%T2 S L "EN% C # O Oi d TT%
TEXT CONTINUATION $"ETOYRC I[S5"EN S N O 0 A TO THE PAPERWORK REDUCTION PROJECT (3150-0104h OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY N AME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR B N 3 0f 8 PILGRIM NUCLEAR POWER STATION 05000-293 93 009 00 TEXT (It more space is required, use additional copies of NRC form 366A)(17)
- Safety-related 4160 VAC Buses A5 and A6 and 480 VAC Buses B1, B2, B6 and its related electrical system were energized. Bus B6 was being powered from Bus B2. The Emergency Diesel Generator 'B' was in standby service. EDG 'A' was not available for service because of maintenance activities.
- The Salt Service Water (SSW) System Loop 'B' pump P-2080 was in service providing cooling water to the RBCCW Loop 'B' heat exchanger. The SSW Loop 'B' pump P-208E was in standby service. The SSW System Loop 'A' pumps were not in service because of Loop 'A' piping replacement. The Loop 'A'/'B' swing pump P-208C was in standby service and available for Loop 'B' service.
- The 345 KV switchyard ring bus was energized via transmission lines 342 and 355. The air type circuit breakers 102, 103, 104 and 105 were closed. The 4160 VAC Buses that were in service were energized via the Startup Transformer.
The Unit Auxiliary and Shutdown Transformers were in standby service.
EVENT DESCRIPTION On May 4, 1993, at 0230 hours0.00266 days <br />0.0639 hours <br />3.80291e-4 weeks <br />8.7515e-5 months <br />, 480 VAC load center Bus B6 became de-energized. The bus became de-energized because circuit breaker 52-102 did not close automatically as designed during a planned transfer conducted while shut down. Circuit breaker 52-102 was manufactured by the General Electric Company, type AK-2A-50-1 modified with a Micro-Versa trip unit.
The transfer was being conducted in accordance with step 4 of procedure 3.M.3-35 (Rev. 14)
Attachment 24, " Automatic Dead Bus Transfer From B2 to 81 Supplying B6 - By Pulling B2 PT Fuses". For this step, the secondary fuses of the potential transformers for Bus 82 were ,
removed from their installed locations. The removal causes the control circuitry to sense ;
a loss of voltage on Bus B2. The removal of the fuses should have resulted in the !
automatic opening of breakers52-202 and 52-602 and the automatic closing of breakers j 52-102 and 52-601. Breaker 52-202 opened but its related transfer breaker (52-102) did >
not close. Meanwhile, breaker 52-602, in-series with breaker 52-202 from Bus B2 to Bus i B6, opened automatically and its related transfer breaker (52-601) closed automatically as l designed. This configuration resulted in safety-related Bus B6 becoming de-energized because the in-series feeder breakers from Bus B2 to Bus B6 were open and one in-series feeder breaker from Bus B1 to B6 was open.
The loss of power to 480 VAC Bus 86 resulted in a loss of power to the following: !
- 480 VAC MCC-810 that provides power to equipment including SSW pump P-208C.
. 480 VAC MCC-B20 that provides power to equipment including: i l
l NRC FORM 3tm @@
i NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPRO'!ED BY OMB NO. 3150-0104 n-m EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS LICENSEE EVENT REPORT (LER) Clu%7'2"mGJ" G B Ro5 EAT O INF M TEXT CONTINUATION $$u" Ness"cISTE"[0A[s[$dN TO THE PAPERWORK REDUCTION PROJECT (31540104), OF FICE OF M ANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) vEAR SOEP "duS?%
4 of 8 PILGRIM NUCLEAR POWER STATION 05000-293 93 009 00 TEXT Of more space is required, use additional copies of NRC Form 366A)(17)
. RHR System Valves:
. Inboard injection valves M0-1001-29A/B (normally closed). This would cause the RHR loops ' A' and 'B' to be inoperable for the Low Pressure Coolant Injection (LPCI) mode.
- Outboard injection valves M0-1001-28A/B (normally open).
. Recirculation System Loops ' A' and 'B' pump suction and discharge valves. This could also cause the RHR/LPCI function to be inoperable.
Breaker 52-102 was closed via its control switch at Bus 81 and Bus B6 was re-energized via Bus B1 at approximately 0235 hours0.00272 days <br />0.0653 hours <br />3.885582e-4 weeks <br />8.94175e-5 months <br />.
Problem Report 93.9215 was written to document the event.
CAUSE Bus B6 became de-energized because breaker 52-102 did not close during the transfer. The cause of breaker 52-102 not closing was a loose wire-to-lug connection in the breaker's control circuit. The wire is located in the time delay portion of the control circuit that permits breaker 52-102 to close automatically. The wire is connected in parallel with the control switch that permits breaker 52-102 to be closed manually. The wire is not lifted and the terminal is not jumpered for Bus B6 transfers.
CORRECTIVE ACTION The lug was replaced and reterminated on May 5,1993. Post work testing was completed with satisfactory results on May 5, 1993, at 0140 hours0.00162 days <br />0.0389 hours <br />2.314815e-4 weeks <br />5.327e-5 months <br />. The testing was conducted in accordance with procedure 3.M.3-35 (Rev. 14) Attachment 24.
The root cause analysis had not been completeo when this report was submitted. If the analysis identifies other corrective actions, the actions will be tracked via the Problem Report process.
SAFETY CONSE0VENCES The de-energizing of 480 VAC Bus 86 posed no threat to the public health and safety.
NRC FORM 366A {5 92)
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NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISslON APPROVEo BY OMB NO. 3150-0104 n-m , EXPIRES 5/31/95 EST1 MATED BURDEN PER RESPONSE TO COMPLY WITH THIS ]
LICENSEE EVENT REPORT (LER) 2""G*"EGOMTERc!M*LAT M RM T TEXT CONTINUATION S u" S
- E E0EN S GT DC 0 1 TO THE PAPERWORK REDUCTON PROJECT (3150-0104), OFFCE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
^
YEAR Ma PILGRIM NUCLEAR POWER STATION 05000-293 93 009 00 TEXT Cf more space is required, use additional copies of NRC Form 366A)(17)
The Core Standby Cooling Systems (CSCS) consist of the High Pressure Coolant Injection (HPCI) System, Automatic Depressurization System (ADS), Core Spray System, and the RHR System /LPCI mode. The HPCI System provides high pressure core cooling. The Core Spray System (Trains ' A' and 'B') and the RHR/LPCI mode are each capable of independently providing low pressure core cooling if necessary. In the event low pressure core cooling was necessary and Bus B6 was or were to become de-energized, the operability of the RHR/LPCI valves, powered by 480 VAC power from Bus B6, would be affected. However, the Core Spray System would be available to provide core cooling by each of the system's two 100 percent capacity Trains ('A' and 'B'). The Core Spray pumps 'A' and 'B' are powered by safety-related 4160 VAC Bus A5 and A6, respectively. The Core Spray Train 'A' suction and injection valves are powered from 480 VAC Bus B1 via MCC-B17. The Core Spray Train
'B' suction and injection valves are powered from 480 VAC Bus B2 via MCC-B18. The Core Spray channel ' A' circuitry is powered from 125 VDC control Bus ' A' via Distribution Panel
'A' (Bus D4). The Core Spray channel 'B' circuitry is powered from 125 VDC control Bus
'B' via Distribution Panel 'B' (Bus DS). This design ensures a failure of one 125 VDC supply would not affect the other power supply and, therefore, the failure would not cause the failure of both Core Spray Trains. Because no loads associated with the Core Spray '
System are connected to Bus B6 or to the 125 VDC Distribution Panel 'C' (Bus D6), a loss of power of Bus B6 or Bus D6 would not cause a failure of either Core Spray Train.
Overload protection is provided on both of the series connected Bus 86 tie breakers52-102 and 52-601 (52-202 and 52-602). Thus, a fault on Bus B1 would not cause the loss of Bus 82 or B6, or a fault on Bus 82 would not cause the loss of Bus 81 or B6. A loss of Bus B6 would not cause the loss of Bus B1 or B2.
This report is submitted in accordance with 10 CFR 50.73(a)(2)(vii)(D) because the normally-closed RHR/LPCI Loops ' A' and 'B' injection valves (MO-1001-29A/B) would not have opened for the RHR/LPCI function and because the normally-open Recirculation System Loops
' A' and 'B' suction and discharge valves would not have closed for the RHR/LPCI function.
For this event, the operability of the RHR/LPCI function was not required.
SIMILARITY TO PREVIOUS EVENTS A review was conducted of Pilgrim Station Licensee Event Reports (LERs). The review focused on LERs involving an instance of Bus B6 becoming similarly de-energimi, or involving a loose wire. The review identified related events reported in LERs 50-293/87-005-00, 90-005-01, and 91-019-00.
LER 87-005-00 involved breaker 52-102 not closing because a jumper was not installed while breaker 52-202 was removed from its cubicle for maintenance. LER 90-005-01 involved the failure of breaker 52-202 to open during a planned transfer of Bus 86. LER 92-019-00 involved the failure of breaker 52-602 to close during a planned transfer of Bus B6. No LERs submitted since 1984 involved a loose wire.
NRC f 04M 3%A (S A1 l
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NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-o1o4 6-m ,
EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS LICENSEE EVENT REPORT (LER) 1 "I 0s"R 2 'f i"Rc T s" M f0 0 N a u %
TEXT CONTINUATION $u"'[TORv cdu'IsEcINlEGTON'"~"*'ssNo"[A$
Dc TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR 6 Of 8 PILGRIM NUCLEAR POWER STATION 05000-293 93 009 00 TEXT (rf more space is required, use additional copies of NRC Form 366A)(17)
For LER 87-005-00, Bus B6 became de-energized while shut down on March 31, 1987 at 0845 hours0.00978 days <br />0.235 hours <br />0.0014 weeks <br />3.215225e-4 months <br /> due to a loss of preferred offsite power (345 KV) during a storm. At the time of the event, Bus B6 was energized from Bus B1 and breaker 52-202 was not installed in its cubicle because it was being overhauled. The EDG 'A' was in standby service and EDG 'B' had been removed from service for planned maintenance. The 345 KV preferred offsite power sources, transmission lines 342 and 355, were energized. The mechanical disconnects for the switchyard air circuit breaker ACB-102 were in the OPEN position because ACB-102 had ,
been removed from service for maintenance. The switchyard air circuit breakers ACB-103, and ACB-104, and ACB-105 were closed. The loss of preferred offsite power resulted in the automatic opening of ACBs 103 and 104 and a loss of voltage to the 4160 VAC Buses, including A5 and A6, and the 480 VAC Buses including B1, B2, and B6. The EDG 'A' started automatically and re-energized Bus A5 and related electrical system as designed approximately 10 seconds later. Meanwhile, the Bus B6 transfer control circuitry, sensing a loss of voltage on Bus B1 for greater than one second, caused breakers52-102 and 52-601 to open automatically. Breaker 52-601 reclosed automatically as a result of Bus B1 becoming re-energized. Concurrently, Bus A6 (and Bus B2) remained de-energized because EDG 'B' was not available for service. Bus B6 remained de-energized and breaker 52-102 did not reclose automatically because a jumper had not been installed in the control circuit when breaker 52-202 was removed from its cubicle for maintenance (overhaul).
After a jumper was installed, breaker 52-102 automatically closed and, with breaker 52-601 in the CLOSED position, Bus B6 was re-energized at 1027 hours0.0119 days <br />0.285 hours <br />0.0017 weeks <br />3.907735e-4 months <br />. The cause of the loss of preferred offsite power was a transmission line 342 fault that was due to the storm. The cause of breaker 52-102 not reclosing was that a detailed review of the control circuitry was not performed while preplanning the removal of breaker 52-202 for maintenance.
For LER 90-005-01, Bus B6 became de-energized during a planned Bus B6 transfer while shut .
down on March 20, 1990 at 1750 hours0.0203 days <br />0.486 hours <br />0.00289 weeks <br />6.65875e-4 months <br />. The transfer was being conducted in accordance with ,
step 4 of procedure 3.M.3-35 (Rev. 10) Attachment 24, " Automatic Dead Bus Transfer From B2 to B1 Supplying B6 - By Pulling B2 PT Fuses". Breaker 52-202 failed to open automatically as designed during the transfer and consequently its related transfer breaker (52-102) did not close. Meanwhile, breaker 52-602 opened as designed and its related transfer breaker (52-601) closed. Consequently, Bus B6 became de-energized because one in-series breaker in each of the two feeder circuits (from Bus B1 to Bus B6 and from Bus B2 to Bus B6) was in the OPEN position. The failure of breaker 52-202 to open resulted in the failure of its trip coil. Bus B2 was intentionally de-energized in response to the event and was re-energized at 1825 hours0.0211 days <br />0.507 hours <br />0.00302 weeks <br />6.944125e-4 months <br /> after breaker 52-202 was tripped and removed from its cubicle.
Breaker 52-202 failed to open because its latch prop, that is part of the breaker's trip mechanism, was misaligned due to the absence of a retainer ring. The cause of the missing retainer ring could not be determined with certainty. Corrective action taken included offsite inspection, overhaul, and testing of breaker 52-202 by the manufacturer, and onsite inspection, overhaul, and testing of similar breakers by manufacturer and utility personnel. Circuit breaker 52-202 was manufactured by the General Electric Company, type AK-2A-50-1 modified with a Micro-Versa trip unit, serial number 224All26-312-AE-1.
NRC FORM 366A (5 94
q, f NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPRO'!ED BY OMB NO. 3150-0104 u-m EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS LICENSEE EVENT REPORT (LER) l%MMEs" RECT S L 1 $ LTMO O J Efe" TEXT CONTINUATION Eu"EORv OcEs's*fw"$S"oT7DC$sso"oN TO THE PAPERWORK REDUCTION PROJECT (3150 0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR M PILGRIM NUCLEAR POWER STATION 05000-293 93 009 00 TEXT pt more space is required, use additionat copies of NRC Form 366A)(17)
For LER 91-019-00, Bus B6 became de-energized during a planned Bus B6 transfer while shut down on May 25, 1991 at 0215 hours0.00249 days <br />0.0597 hours <br />3.554894e-4 weeks <br />8.18075e-5 months <br />. Breaker 52-602 did not close automatically as designed during the transfer. The transfer was being conducted in accordance with step 4 of procedure 3.M.3-35 (Rev. 12) Attachment 23, " Automatic Dead Bus Transfer From Bl to B2 Supplying B6 - By Pulling B1 PT Fuses". For the step, the secondary fuses of the potential transformers for Bus B1 were removed from their installed locations. The removal of the fuses should have resulted in the automatic opening of breakers52-102 and 52-601, and the automatic closing of breakers52-202 and 52-602. Breaker 52-601 opened -
automatically but breaker 52-602 did not close. Meanwhile, breaker 52-102 opened -
automatically and its related transfer breaker 52-202 closed automatically as designed.
This configuration resulted in Bus B6 becoming de-energized because breakers52-102 and 52-601 from Bus Bl to Bus B6 were open, and breaker 52-602 from Bus B2 to Bus B6 was open.
The cause of breaker 52-602 not closing was interference between the breaker trip latch roller assembly and clevis pin. The interference was similar to that documented in Service Advice Letter (SAL) 306.0, issued on May 1, 1991. A 10 CFR Part 21 report regarding the breaker was submitted to the NRC on July 26, 1991. Corrective action taken included breaker repair by General Electric personnel. The repair included machining the trip latch roller assembly and clevis pin to establish the clearance described in SAL 306.0. Circuit breaker 52-602 was manufactured by the General Electric Company, type AK-2A-50-1 modified with a Micro-Versa trip unit, serial number 0224A1126-310-AE-2.
ENERGY INDUSTRY IDENTIFICATION SYSTEM (Ells) CODES The Ells codes for this report are as follows:
COMPONENTS CODES Bus BU Circuit Breaker (52-102), AC 52 SYSTEMS Low-Voltage Power System EC Residual Heat Removal System (RHR/LPCI) B0 NAC FORM 304A (5 9?)
Tl T I
i NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO,3150-0104 I t s-m EXPIRES 5/31/95
, j EST! MATED BURDEN PER HESPONSE TO COMPLY WTTH THIS INFORMATON COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) COMMENT 3 REGARDING BURDEN EST! MATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MN98 7714), U.S. NUCLEAR TEXT CONTINUATION REGULATORY COMMISSON, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTON PRuJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
SEQUENTIAL REVISION vEAR NuusER NuuseR PILGRIM NUCLEAR POWER STATION 05000-293 8d8 93 009 00 TEXT (tt more space is required, use additional copies of NRC Form 366A)(17) l STATICN ,
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