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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046C3131993-07-28028 July 1993 LER 93-015-00:on 930630,HPCI Sys Declared Inoperable Due to Indicated Flow During Surveillance.Caused by Foreign Matl That Plugged Portion of Restricting Orifice.Restricting Orifice Removed,Cleaned & reinstalled.W/930728 Ltr ML20046B5241993-07-26026 July 1993 LER 93-007-01:on 930317,automatic Closing of RCIC Sys Turbine Steam Supply Isolation Valves Occurred Due to High Steam Flow Signal.Increased Frequency of Valve Testing from Monthly to weekly.W/930726 Ltr ML20045F8601993-06-30030 June 1993 LER 93-014-00:on 930531,automatic Scram Occurred,Resulting from Operation of Auxiliary Transformer Differential Relay During Power Ascension.Uat Phase B & C Differential Relays Left Interchanged as Investigative aid.W/930630 Ltr ML20045E2301993-06-25025 June 1993 LER 93-013-00:on 930530,RCIC Sys Declared Inoperable & 7 Day TS 3.5.D.2 LCO Entered Due to Speed Oscillations Which Occurred After Several Minutes of steady-state Operation. Caused by Actuator Failure.Actuator replaced.W/930625 Ltr ML20045E2251993-06-25025 June 1993 LER 93-012-00:on 930529,unplanned PCIS Group I Isolation Signal Occurred While Opening MSIV During Startup,Resulting in Automatic Closing of Related Valves.Caused by Licensed Operator Error.Group 1 Isolation reset.W/930625 Ltr ML20045D6941993-06-23023 June 1993 LER 93-011-00:on 930525,determined That Initial as-found Popping Pressures of Pilot Valves for Three Target Rock Main Steam Relief Valves Out of TS Tolerance.Caused by Setpoint Drift.Valves Reworked & Reassembled by Target Rock Corp ML20045D1861993-06-18018 June 1993 LER 93-010-00:on 930519,SUT Became de-energized During Planned Calibr of Turbine/Generator Relays Lockout Test While Shut Down.Caused by Personnel Error.Discussion Conducted W/Personnel Re Attention to detail.W/930618 Ltr ML20044H0441993-06-0202 June 1993 LER 93-009-00:on 930504,circuit Breaker Did Not Close During Planned Bus Transfer Due to Loose Control Circuit Wire.Lug Replaced & Reterminated on 930505 & Post Work Testing Completed W/Satisfactory results.W/930602 Ltr ML20024G7451991-04-24024 April 1991 LER 91-005-00:on 910325,diesel Generator Inoperable,Causing Loss of Ac Power to Train B Components of Safety Sys & Actuating Portions of Primary/Secondary Containment Sys. Caused by Voltage Regulator failure.W/910424 Ltr ML20029A6721991-02-25025 February 1991 LER 91-001-00:on 910125,automatic Primary Containment Isolation Control Sys Group 5 Actuation Occurred,Resulting in Closing of RCIC Turbine Steam Supply Isolation Valves. Caused by High Flow conditions.W/910225 Ltr ML20028G9731990-09-20020 September 1990 LER 89-036-01:on 891122,determined That HPCI Sys Inoperable Due to Inoperable Gland Seal Condenser Blower Motor.Caused by age-related Wear of Motor.Blower Motor Replaced & Blower Tested W/Satisfactory results.W/900920 Ltr ML20028G9121990-09-18018 September 1990 LER 89-037-01:on 891130,primary Containment/Traversing in-core Probe Ball Valve Discovered to Be Almost Full Open. Caused by Damage to Valve Stem Due to Manual Manipulation of Stem.Ball Valve & Solenoid Actuator replaced.W/900918 Ltr ML20043G3541990-06-12012 June 1990 LER 90-008-00:on 900513,automatic Scram Resulting from Load Rejection Occurred While at Full Power,Resulting in Trip of Generator Field Breakers.Caused by Fault on Offsite 345 Kv Transmission sys.Loss-of-field Relay replaced.W/900612 Ltr ML20043F8291990-06-0606 June 1990 LER 90-007-00:on 900507,discovered That Drywell to Suppression Chamber Vacuum Breaker Surveillance Not Performed Prior to Startup in 1988.Caused by Misunderstanding of requirements.W/900606 Ltr ML20042F5911990-04-30030 April 1990 LER 90-006-00:on 900330,determined That Position of Primary Containment Sys Isolation Valve Not Recorded Daily,Per Tech Specs.Review Performed to Determine If Other Problems Existed.Plant Shut Down & Review performed.W/900430 Ltr ML20012F5751990-04-0606 April 1990 LER 90-003-00:on 900311,automatic Actuation of Main Steam Sys Group 1 Portion of Primary Containment Isolation Control Sys Occurred.Caused by False High Reactor Vessel Water Level Signal.Procedure Developed Re backfill.W/900406 Ltr ML20012E9831990-03-30030 March 1990 LER 90-002-00:on 900228,determined That Max Fraction of Limiting Power Density Not Checked Daily During Reactor Power Operation,Per Tech Spec 4.1.B.On 900323,addl Tech Spec Issue Discovered.Tech Specs changed.W/900330 Ltr ML20012C4871990-03-12012 March 1990 LER 90-001-00:on 900209,24 H Limiting Condition for Operation Entered When Two RCS Instrumentation Excess Flow Check Valves Inappropriately Verified Operable During Testing.Cause Undetermined.Two Valves replaced.W/900312 Ltr ML20005G0981990-01-0808 January 1990 LER 89-038-00:on 891208,unplanned Automatic Reactor Protection Sys Scram Signal & Reactor Scram Occurred.Caused by False Low Reactor Vessel Water Level Signal.Local Level Indicators Satisfactorily calibr.W/900108 Ltr ML20005F8481990-01-0808 January 1990 LER 89-039-00:on 891209,automatic Actuation of RHR Sys Portion of Primary Containment Isolation Control Sys Occurred.Caused by Hydrodynamic Transient That Actuated Protective High Pressure switches.W/900108 Ltr ML20005E8551989-12-30030 December 1989 LER 89-037-00:on 891130,discovered That Traversing in-core Probe Ball Valve,Mfg by Consolidated Controls,Inc,Closed,In Violation of Tech Specs.Caused by Damage to Valve Stem.Ball Valve & Actuator replaced.W/891230 Ltr ML20011D1361989-12-11011 December 1989 LER 89-035-00:on 891111,inadvertent Actuation of Portion of Secondary Containment Sys During Surveillance Testing Occurred.Caused by Location of Radiation Isolation Control Sys Channel a Logic Relay.Procedure revised.W/891211 Ltr ML20005D7421989-12-0606 December 1989 LER 89-033-00:on 891106,automatic Actuation of Group 1 Portion of Primary Containment Isolation Control Sys (PCIS) Occurred.Caused by High Reactor Vessel Water Level.Manual Valve Closed & PCIS Logic Circuitry reset.W/891206 Ltr ML19351A4581989-12-0606 December 1989 LER 89-034-00:on 891108,determined That Reactor Pressure Exceeded 150 Psig on 891107 W/O Performing Surveillance Procedure 8.5.4.4, HPCI Valve Operability Test. Caused by Personnel Error.Procedure initiated.W/891206 Ltr ML19332D1421989-11-22022 November 1989 LER 89-031-00:on 891024,closing Times for Two in-series Primary Containment Isolation Valves Exceeded Acceptance Criteria During Shutdown Testing.Cause Undetermined.Closing Time Retested W/Satisfactory results.W/891122 Ltr ML19332D6231989-11-20020 November 1989 LER 89-032-00:on 891020,pneumatic Pressure Drop for Two of Four Automatic Depressurization Sys Accumulators Discovered Greater than Max Acceptable Value.Caused by Leakage from Seat of Supply Check Valves.Seat replaced.W/891120 Ltr ML19324C3181989-11-0909 November 1989 LER 88-002-01:on 880117,full Reactor Protection Sys Scram Trip Signal Occurred During Surveillance Test,Resulting in Incomplete Actuations.Caused by Procedure Inadequacy.Logic Relay Replaced & Procedure revised.W/891109 Ltr ML19324B1131989-10-21021 October 1989 LER 89-030-00:on 890926,control Room High Efficiency Air Filtration Sys Flowrate non-conservative Due to Procedure Error.Caused by Transcription Error.Procedure Revised & Test Reperformed Using Corrected procedure.W/891021 Ltr ML19325D4681989-10-16016 October 1989 LER 89-029-00:on 890914,locked High Radiation Area Door Found to Have Been Unsecured Contrary to Tech Spec 6.13.2. Caused by Failure to Adhere to Approved Procedures. Training on Access Requirements initiated.W/891016 Ltr ML19325D1861989-10-10010 October 1989 LER 89-028-00:on 890907,HPCI Sys Declared Inoperable Because Mechanical Overspeed Trip Occurred During Surveillance Test. Caused by Failure of Ramp Generator Signal Converter Module. Module Removed & Sent to Mfg for exam.W/891010 Ltr ML17277B8221984-07-20020 July 1984 LER 82-049/01X-1:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting.Caused by Personnel Error.Valve Removed & Replaced W/Properly Set Spare Valve. Procedure revised.W/840720 Ltr ML20024C3231983-06-24024 June 1983 Updated LER 82-038/03X-1:on 820817,RCIC Steam Line High Differential Pressure Alarm Received.Caused by Air in Sensing Lines to Pressure Switches.Cross Threaded Cap Found on in-line Snubber.Snubber replaced.W/830624 Ltr ML20024C2211983-06-24024 June 1983 Updated LER 80-053/03X-1:on 800814,0907 & 14,HPCI Turbine Exhaust Line Snubber 23-3-36 Determined Inoperable.Caused by Transient Hydrodynamic Shock During Startup & Shutdown. Snubbers upgraded.W/830624 Ltr ML20024B8451983-06-24024 June 1983 LER 83-031/03L-0:on 830528,HPCI Sys Made Inoperable to Repair Steam Leak on AO 2301-31.Caused by Leaking Stem Packing.Packing Replaced.Valve Tested Satisfactorily.Sys Returned to svc.W/830624 Ltr ML20024B8321983-06-24024 June 1983 LER 83-030/03L-0:on 830527,both HPCI Area Smoke Detection Sys Alarmed in Main Control Room.Caused by Valve A02301-31 Steam Leak Causing False Indications.Valve repaired.W/830624 Ltr ML20024C3101983-06-21021 June 1983 Updated LER 79-007/03X-1:on 790212,while Performing Test 8.7.4.3,valves AO-5033A,CV-5065-10,15,16 & 17 Failed to Give Proper Position Indication When Cycled & to Close within Specified Tolerance.Cause Not stated.W/830621 Ltr ML20024A8861983-06-16016 June 1983 LER 83-027/03L-0:on 830518,during Routine Insp,Folding Fire Door Found Inoperable.Caused by Operating Cable Becoming Detached from Pulley Due to Slack.Cable Reattached & Operating Mechanism adjusted.W/830616 Ltr ML20023D1691983-05-0909 May 1983 Updated LER 82-008/01X-1:on 820331,HPCI Injection Valve MO-2301-8 Failed to Open in Required Manner.Caused by Missing Wire Jumper Intended to Bypass Motor Operator Torque Switch.Jumper Installed & Valve Tested Satisfactorily ML20023D0671983-05-0909 May 1983 LER 83-021/03L-0:on 830411,during Surveillance Test 8.7.4.3, Primary Containment Isolation Valve AO-5033B Failed to Meet 10-s Closing Time Requirements.Caused by Lubricant Infiltrating Solenoid Valve Components.Components Replaced ML20023D0181983-05-0404 May 1983 LER 83-022/03L-0:on 830413,overload on Valve Motor 1301-17 Resulted in Loss of High Pressure Core Cooling Backup Capability.Caused by Oxidation in Motor End Bell & Motor Brushes,Due to Humidity Caused by Leaking Valve Packing ML20028G1591983-01-28028 January 1983 LER 83-002/01T-0:on 830116,flow Ref off-normal Alarm Received.Average Power Range Monitor Flux Scram Trip Settings Affected.Cause Under Investigation.Flow Inputs Monitored & Amplifier B Recalibr ML20028F4121983-01-17017 January 1983 LER 83-002/01X-0:on 830116,while Clearing off-normal Alarm for Flow Comparators,Average Power Range Monitor Flux Scram Trip Settings Found in Nonconservative Direction.Caused by Drifting Proportional Amplifiers.Settings Checked Daily ML20028B0421982-11-16016 November 1982 LER 82-049/01T-0:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting of 1240 Psig, Exceeding Tech Specs.Caused by Personnel Error.Set Valve Removed,Procedure Adherence Stressed & Procedure Revised ML20027C9801982-10-20020 October 1982 LER 82-039/03L-0:on 820920,timing Tests of Three Reactor Water Cleanup Isolation Valves 1201-2,-5 & -80 Not Completed within Allowed Time.Caused by Operational Constraints Requiring Testing at Reduced Power ML20027C9941982-10-20020 October 1982 LER 82-040/03L-0:on 820920,found Reactor Protection Sys Initiation Function of Turbine Stop Valve Completed 1 Day Late.Caused by Decision to Defer Test Due to MSIV D Line Isolation.Tracking Sys Implemented to Prevent Recurrences ML20052B9141982-04-23023 April 1982 LER 82-010/03L-0:on 820326,during Review of Testing Requirements,Surveillance Test 8.I.4 Standby Liquid Control Sys Found Not Verified.Caused by Breakdown in Multidiscipline Review of Results ML20052F2071982-04-14014 April 1982 Updated LER 81-060/03X-1:on 811020,determined Potential Exists to Reduce Number of Operable APRM & IRM Instrument Channels in Rod Block Trip Sys to Below Tech Spec Min ML20050A6321982-03-19019 March 1982 Updated LER 82-055/01T-1:on 810926,during Shutdown,Yarway Level Indicators Started Oscillating.Drywell Temp Was 240 F at 81-ft W/Elevation Coolant Temp 220 F.Caused by Ineffective Drywell Cooling.Ventilation Returned to Svc ML20050A4521982-03-19019 March 1982 LER 82-006/01T-0:on 820304,while Performing Maint Re SIL 352 on Pressure Adjustment Mechanism HPCI Stop Valve,Three Broken cap-screws Found.No Cause Determined.Screws Examined, Replaced & Sys Returned to Svc ML20050A4331982-03-19019 March 1982 Updated LER 81-062/01X-1:on 811116,Wyle Labs Informed Util That Two Target Rock Safety Relief Valves Had Not Passed Setpoint Tests.Caused by Setpoint Shift Due to Changes to Designed Differential Forces from Excessive Pilot Leakage 1993-07-28
[Table view] Category:RO)
MONTHYEARML20046C3131993-07-28028 July 1993 LER 93-015-00:on 930630,HPCI Sys Declared Inoperable Due to Indicated Flow During Surveillance.Caused by Foreign Matl That Plugged Portion of Restricting Orifice.Restricting Orifice Removed,Cleaned & reinstalled.W/930728 Ltr ML20046B5241993-07-26026 July 1993 LER 93-007-01:on 930317,automatic Closing of RCIC Sys Turbine Steam Supply Isolation Valves Occurred Due to High Steam Flow Signal.Increased Frequency of Valve Testing from Monthly to weekly.W/930726 Ltr ML20045F8601993-06-30030 June 1993 LER 93-014-00:on 930531,automatic Scram Occurred,Resulting from Operation of Auxiliary Transformer Differential Relay During Power Ascension.Uat Phase B & C Differential Relays Left Interchanged as Investigative aid.W/930630 Ltr ML20045E2301993-06-25025 June 1993 LER 93-013-00:on 930530,RCIC Sys Declared Inoperable & 7 Day TS 3.5.D.2 LCO Entered Due to Speed Oscillations Which Occurred After Several Minutes of steady-state Operation. Caused by Actuator Failure.Actuator replaced.W/930625 Ltr ML20045E2251993-06-25025 June 1993 LER 93-012-00:on 930529,unplanned PCIS Group I Isolation Signal Occurred While Opening MSIV During Startup,Resulting in Automatic Closing of Related Valves.Caused by Licensed Operator Error.Group 1 Isolation reset.W/930625 Ltr ML20045D6941993-06-23023 June 1993 LER 93-011-00:on 930525,determined That Initial as-found Popping Pressures of Pilot Valves for Three Target Rock Main Steam Relief Valves Out of TS Tolerance.Caused by Setpoint Drift.Valves Reworked & Reassembled by Target Rock Corp ML20045D1861993-06-18018 June 1993 LER 93-010-00:on 930519,SUT Became de-energized During Planned Calibr of Turbine/Generator Relays Lockout Test While Shut Down.Caused by Personnel Error.Discussion Conducted W/Personnel Re Attention to detail.W/930618 Ltr ML20044H0441993-06-0202 June 1993 LER 93-009-00:on 930504,circuit Breaker Did Not Close During Planned Bus Transfer Due to Loose Control Circuit Wire.Lug Replaced & Reterminated on 930505 & Post Work Testing Completed W/Satisfactory results.W/930602 Ltr ML20024G7451991-04-24024 April 1991 LER 91-005-00:on 910325,diesel Generator Inoperable,Causing Loss of Ac Power to Train B Components of Safety Sys & Actuating Portions of Primary/Secondary Containment Sys. Caused by Voltage Regulator failure.W/910424 Ltr ML20029A6721991-02-25025 February 1991 LER 91-001-00:on 910125,automatic Primary Containment Isolation Control Sys Group 5 Actuation Occurred,Resulting in Closing of RCIC Turbine Steam Supply Isolation Valves. Caused by High Flow conditions.W/910225 Ltr ML20028G9731990-09-20020 September 1990 LER 89-036-01:on 891122,determined That HPCI Sys Inoperable Due to Inoperable Gland Seal Condenser Blower Motor.Caused by age-related Wear of Motor.Blower Motor Replaced & Blower Tested W/Satisfactory results.W/900920 Ltr ML20028G9121990-09-18018 September 1990 LER 89-037-01:on 891130,primary Containment/Traversing in-core Probe Ball Valve Discovered to Be Almost Full Open. Caused by Damage to Valve Stem Due to Manual Manipulation of Stem.Ball Valve & Solenoid Actuator replaced.W/900918 Ltr ML20043G3541990-06-12012 June 1990 LER 90-008-00:on 900513,automatic Scram Resulting from Load Rejection Occurred While at Full Power,Resulting in Trip of Generator Field Breakers.Caused by Fault on Offsite 345 Kv Transmission sys.Loss-of-field Relay replaced.W/900612 Ltr ML20043F8291990-06-0606 June 1990 LER 90-007-00:on 900507,discovered That Drywell to Suppression Chamber Vacuum Breaker Surveillance Not Performed Prior to Startup in 1988.Caused by Misunderstanding of requirements.W/900606 Ltr ML20042F5911990-04-30030 April 1990 LER 90-006-00:on 900330,determined That Position of Primary Containment Sys Isolation Valve Not Recorded Daily,Per Tech Specs.Review Performed to Determine If Other Problems Existed.Plant Shut Down & Review performed.W/900430 Ltr ML20012F5751990-04-0606 April 1990 LER 90-003-00:on 900311,automatic Actuation of Main Steam Sys Group 1 Portion of Primary Containment Isolation Control Sys Occurred.Caused by False High Reactor Vessel Water Level Signal.Procedure Developed Re backfill.W/900406 Ltr ML20012E9831990-03-30030 March 1990 LER 90-002-00:on 900228,determined That Max Fraction of Limiting Power Density Not Checked Daily During Reactor Power Operation,Per Tech Spec 4.1.B.On 900323,addl Tech Spec Issue Discovered.Tech Specs changed.W/900330 Ltr ML20012C4871990-03-12012 March 1990 LER 90-001-00:on 900209,24 H Limiting Condition for Operation Entered When Two RCS Instrumentation Excess Flow Check Valves Inappropriately Verified Operable During Testing.Cause Undetermined.Two Valves replaced.W/900312 Ltr ML20005G0981990-01-0808 January 1990 LER 89-038-00:on 891208,unplanned Automatic Reactor Protection Sys Scram Signal & Reactor Scram Occurred.Caused by False Low Reactor Vessel Water Level Signal.Local Level Indicators Satisfactorily calibr.W/900108 Ltr ML20005F8481990-01-0808 January 1990 LER 89-039-00:on 891209,automatic Actuation of RHR Sys Portion of Primary Containment Isolation Control Sys Occurred.Caused by Hydrodynamic Transient That Actuated Protective High Pressure switches.W/900108 Ltr ML20005E8551989-12-30030 December 1989 LER 89-037-00:on 891130,discovered That Traversing in-core Probe Ball Valve,Mfg by Consolidated Controls,Inc,Closed,In Violation of Tech Specs.Caused by Damage to Valve Stem.Ball Valve & Actuator replaced.W/891230 Ltr ML20011D1361989-12-11011 December 1989 LER 89-035-00:on 891111,inadvertent Actuation of Portion of Secondary Containment Sys During Surveillance Testing Occurred.Caused by Location of Radiation Isolation Control Sys Channel a Logic Relay.Procedure revised.W/891211 Ltr ML20005D7421989-12-0606 December 1989 LER 89-033-00:on 891106,automatic Actuation of Group 1 Portion of Primary Containment Isolation Control Sys (PCIS) Occurred.Caused by High Reactor Vessel Water Level.Manual Valve Closed & PCIS Logic Circuitry reset.W/891206 Ltr ML19351A4581989-12-0606 December 1989 LER 89-034-00:on 891108,determined That Reactor Pressure Exceeded 150 Psig on 891107 W/O Performing Surveillance Procedure 8.5.4.4, HPCI Valve Operability Test. Caused by Personnel Error.Procedure initiated.W/891206 Ltr ML19332D1421989-11-22022 November 1989 LER 89-031-00:on 891024,closing Times for Two in-series Primary Containment Isolation Valves Exceeded Acceptance Criteria During Shutdown Testing.Cause Undetermined.Closing Time Retested W/Satisfactory results.W/891122 Ltr ML19332D6231989-11-20020 November 1989 LER 89-032-00:on 891020,pneumatic Pressure Drop for Two of Four Automatic Depressurization Sys Accumulators Discovered Greater than Max Acceptable Value.Caused by Leakage from Seat of Supply Check Valves.Seat replaced.W/891120 Ltr ML19324C3181989-11-0909 November 1989 LER 88-002-01:on 880117,full Reactor Protection Sys Scram Trip Signal Occurred During Surveillance Test,Resulting in Incomplete Actuations.Caused by Procedure Inadequacy.Logic Relay Replaced & Procedure revised.W/891109 Ltr ML19324B1131989-10-21021 October 1989 LER 89-030-00:on 890926,control Room High Efficiency Air Filtration Sys Flowrate non-conservative Due to Procedure Error.Caused by Transcription Error.Procedure Revised & Test Reperformed Using Corrected procedure.W/891021 Ltr ML19325D4681989-10-16016 October 1989 LER 89-029-00:on 890914,locked High Radiation Area Door Found to Have Been Unsecured Contrary to Tech Spec 6.13.2. Caused by Failure to Adhere to Approved Procedures. Training on Access Requirements initiated.W/891016 Ltr ML19325D1861989-10-10010 October 1989 LER 89-028-00:on 890907,HPCI Sys Declared Inoperable Because Mechanical Overspeed Trip Occurred During Surveillance Test. Caused by Failure of Ramp Generator Signal Converter Module. Module Removed & Sent to Mfg for exam.W/891010 Ltr ML17277B8221984-07-20020 July 1984 LER 82-049/01X-1:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting.Caused by Personnel Error.Valve Removed & Replaced W/Properly Set Spare Valve. Procedure revised.W/840720 Ltr ML20024C3231983-06-24024 June 1983 Updated LER 82-038/03X-1:on 820817,RCIC Steam Line High Differential Pressure Alarm Received.Caused by Air in Sensing Lines to Pressure Switches.Cross Threaded Cap Found on in-line Snubber.Snubber replaced.W/830624 Ltr ML20024C2211983-06-24024 June 1983 Updated LER 80-053/03X-1:on 800814,0907 & 14,HPCI Turbine Exhaust Line Snubber 23-3-36 Determined Inoperable.Caused by Transient Hydrodynamic Shock During Startup & Shutdown. Snubbers upgraded.W/830624 Ltr ML20024B8451983-06-24024 June 1983 LER 83-031/03L-0:on 830528,HPCI Sys Made Inoperable to Repair Steam Leak on AO 2301-31.Caused by Leaking Stem Packing.Packing Replaced.Valve Tested Satisfactorily.Sys Returned to svc.W/830624 Ltr ML20024B8321983-06-24024 June 1983 LER 83-030/03L-0:on 830527,both HPCI Area Smoke Detection Sys Alarmed in Main Control Room.Caused by Valve A02301-31 Steam Leak Causing False Indications.Valve repaired.W/830624 Ltr ML20024C3101983-06-21021 June 1983 Updated LER 79-007/03X-1:on 790212,while Performing Test 8.7.4.3,valves AO-5033A,CV-5065-10,15,16 & 17 Failed to Give Proper Position Indication When Cycled & to Close within Specified Tolerance.Cause Not stated.W/830621 Ltr ML20024A8861983-06-16016 June 1983 LER 83-027/03L-0:on 830518,during Routine Insp,Folding Fire Door Found Inoperable.Caused by Operating Cable Becoming Detached from Pulley Due to Slack.Cable Reattached & Operating Mechanism adjusted.W/830616 Ltr ML20023D1691983-05-0909 May 1983 Updated LER 82-008/01X-1:on 820331,HPCI Injection Valve MO-2301-8 Failed to Open in Required Manner.Caused by Missing Wire Jumper Intended to Bypass Motor Operator Torque Switch.Jumper Installed & Valve Tested Satisfactorily ML20023D0671983-05-0909 May 1983 LER 83-021/03L-0:on 830411,during Surveillance Test 8.7.4.3, Primary Containment Isolation Valve AO-5033B Failed to Meet 10-s Closing Time Requirements.Caused by Lubricant Infiltrating Solenoid Valve Components.Components Replaced ML20023D0181983-05-0404 May 1983 LER 83-022/03L-0:on 830413,overload on Valve Motor 1301-17 Resulted in Loss of High Pressure Core Cooling Backup Capability.Caused by Oxidation in Motor End Bell & Motor Brushes,Due to Humidity Caused by Leaking Valve Packing ML20028G1591983-01-28028 January 1983 LER 83-002/01T-0:on 830116,flow Ref off-normal Alarm Received.Average Power Range Monitor Flux Scram Trip Settings Affected.Cause Under Investigation.Flow Inputs Monitored & Amplifier B Recalibr ML20028F4121983-01-17017 January 1983 LER 83-002/01X-0:on 830116,while Clearing off-normal Alarm for Flow Comparators,Average Power Range Monitor Flux Scram Trip Settings Found in Nonconservative Direction.Caused by Drifting Proportional Amplifiers.Settings Checked Daily ML20028B0421982-11-16016 November 1982 LER 82-049/01T-0:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting of 1240 Psig, Exceeding Tech Specs.Caused by Personnel Error.Set Valve Removed,Procedure Adherence Stressed & Procedure Revised ML20027C9801982-10-20020 October 1982 LER 82-039/03L-0:on 820920,timing Tests of Three Reactor Water Cleanup Isolation Valves 1201-2,-5 & -80 Not Completed within Allowed Time.Caused by Operational Constraints Requiring Testing at Reduced Power ML20027C9941982-10-20020 October 1982 LER 82-040/03L-0:on 820920,found Reactor Protection Sys Initiation Function of Turbine Stop Valve Completed 1 Day Late.Caused by Decision to Defer Test Due to MSIV D Line Isolation.Tracking Sys Implemented to Prevent Recurrences ML20052B9141982-04-23023 April 1982 LER 82-010/03L-0:on 820326,during Review of Testing Requirements,Surveillance Test 8.I.4 Standby Liquid Control Sys Found Not Verified.Caused by Breakdown in Multidiscipline Review of Results ML20052F2071982-04-14014 April 1982 Updated LER 81-060/03X-1:on 811020,determined Potential Exists to Reduce Number of Operable APRM & IRM Instrument Channels in Rod Block Trip Sys to Below Tech Spec Min ML20050A6321982-03-19019 March 1982 Updated LER 82-055/01T-1:on 810926,during Shutdown,Yarway Level Indicators Started Oscillating.Drywell Temp Was 240 F at 81-ft W/Elevation Coolant Temp 220 F.Caused by Ineffective Drywell Cooling.Ventilation Returned to Svc ML20050A4521982-03-19019 March 1982 LER 82-006/01T-0:on 820304,while Performing Maint Re SIL 352 on Pressure Adjustment Mechanism HPCI Stop Valve,Three Broken cap-screws Found.No Cause Determined.Screws Examined, Replaced & Sys Returned to Svc ML20050A4331982-03-19019 March 1982 Updated LER 81-062/01X-1:on 811116,Wyle Labs Informed Util That Two Target Rock Safety Relief Valves Had Not Passed Setpoint Tests.Caused by Setpoint Shift Due to Changes to Designed Differential Forces from Excessive Pilot Leakage 1993-07-28
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217E3021999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Pilgrim Nuclear Station.With ML20212C2921999-09-16016 September 1999 SER Accepting Licensee Request for Relief from ASME Code Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Pilgrim Nuclear Power Station ML20216F3511999-09-0808 September 1999 ISI Summary Rept for Refuel Outage 12 at Pnps ML20216E6881999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pilgrim Nuclear Power Station.With ML20210R3401999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Pilgrim Nuclear Power Station.With ML20209C4731999-07-0707 July 1999 Addendum to SE on Proposed Transfer of Operating License & Matls License from Boston Edison Co to Entergy Nuclear Generation Co ML20209H8251999-07-0101 July 1999 Provides Commission with Evaluation of & Recommendations for Improvement in Processes Used in Staff Review & Approval of Applications for Transfer of Operating Licenses of TMI-1 & Pilgrim Station ML20209E6191999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Pilgrim Nuclear Power Station.With ML20196H2451999-06-29029 June 1999 SER Denying Licensee Proposed Alternative in Relief Request PRR-13,rev 2.Staff Determined That Proposed Alternative Provides Insufficient Info to Determine Adequacy of Scope of Implementation ML20209A8901999-06-28028 June 1999 SER Accepting Licensee Proposed Alternative to Use Code Case N-573 for Remainder of 10-year Interval Pursuant to 10CFR50.55a(a)(3)(i) ML20209B9861999-06-23023 June 1999 Rev 13A to Pilgrim Nuclear Power Station COLR for Cycle 13 ML20217N9061999-06-21021 June 1999 Rept of Changes,Tests & Experiments for Period of 970422-990621 ML20195K3431999-06-15015 June 1999 Safety Evaluation Granting Licensee Request to Use Guidance of GL 90-05 to Repair Flaws in ASME Class 3 Salt Svc Water System Piping for Plant ML20195G8231999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Pnps.With ML20207E7471999-05-27027 May 1999 Safety Evaluation Granting Request Re Reduction of IGSCC Insp of Category D Welds Due to Implementation of HWC to License DPR-35 ML20206M1971999-05-11011 May 1999 SER Accepting Request for Approval to Repair Flaws in ASME Code Class 3 Salt Svc Water Piping at Plant ML20206J6611999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Pilgrim Nuclear Power Station.With ML20205L0221999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Pilgrim Nuclear Power Station.With ML20207J5471999-03-0909 March 1999 Training Simulator,1999 4-Yr Certification Rept ML20207F9401999-03-0101 March 1999 Long Term Program Semi-Annual Rept for Pilgrim Nuclear Power Station ML20207H5451999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Pilgrim Nuclear Power Station.With ML20196E2151998-12-31031 December 1998 1998 Annual Rept for Boston Edison & Securities & Exchange Commission Form 10-K Rept.With ML20206Q2741998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Pilgrim Nuclear Power Station.With ML20197J3591998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Pilgrim Nuclear Power Station.With ML20195C9951998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Pilgrim Nuclear Power Station.With ML20154K0721998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Pilgrim Nuclear Power Station.With ML20153D3901998-09-22022 September 1998 Safety Evaluation Granting 970707 Request to Use Guidance in GL 90-05 to Repair Flaws in ASME Class 3 Salt Svc Water Sys Piping for Pilgrim Nuclear Power Station ML20197C5011998-09-0404 September 1998 Rev 12C,Pages 4 & 5 to Pilgrim Nuclear Power Station Colr ML20197C5471998-08-31031 August 1998 Rev 12C to Pilgrim Nuclear Power Station Colr ML20151W8231998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Pilgrim Nuclear Power Station.With ML20237E2251998-08-26026 August 1998 Suppl & Revs to SE for Amend 173 for Pigrim Nuclear Power Station ML20237A9941998-07-31031 July 1998 Monthly Operating Rept for Pilgrim Nuclear Power Station ML20236U8201998-07-13013 July 1998 Rev 12B to Pilgrim Nuclear Power Station COLR (Cycle 12) ML20236P0151998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Pilgrim Nuclear Power Station ML20249A3741998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Pilgrim Nuclear Power Station.W/Undated Ltr ML20247H2081998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Pilgrim Nuclear Power Station ML20207B7601998-03-31031 March 1998 Final Rept, Pilgrim Nuclear Power Station Site-Specific Offsite Radiological Emergency Preparedenss Prompt Alert & Notification System Quality Assurance Verification, Prepared for FEMA ML20216G3911998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Pilgrim Nuclear Power Station ML20216J3741998-03-19019 March 1998 Safety Evaluation Accepting Licensee Request to Evaluate Elevated Tailpipe Temp on Safety Relief Valve SRV 203-3B ML20248L2241998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Pilgrim Nuclear Station ML20202G5251998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Pilgrim Nuclear Power Station ML20236M8511997-12-31031 December 1997 1997 Annual Rept for Boston Edison & Securities & Exchange Commission Form 10-K Rept ML20198L7701997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Pilgrim Nuclear Power Station ML20203D6101997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Pilgrim Nuclear Power Station ML20202D5761997-11-0808 November 1997 1997 Evaluated Exercise BECO-LTR-97-111, Monthly Operating Rept for Oct 1997 for Pilgrim Nuclear Power Station1997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Pilgrim Nuclear Power Station ML20217D6431997-10-0101 October 1997 Safety Evaluation Granting Request for Approval to Repair Flaws in Accordance W/Gl 90-05 for ASME Class 3 SSW Piping for Pilgrim ML20217H5621997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Pilgrim Nuclear Power Station ML20216J4131997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Pilgrim Nuclear Power Station ML20210J3321997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Pilgrim Nuclear Power Station 1999-09-08
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_ _ _ _ - - _ _ . . . . . . .
Ry 10 CFR 50.73 V s. .
c .
BO$1DNED6CN Pilgrim Nuclear Power station
.. Rocky Hill Road Plymouth, Massachusetts 02360 Ralph G. Bird
, senior Vice President - Nuclear December 6, 1989
- c BECo Ltr. 89 172 U.S. Nuclear Regulatory Commission
-Attn: Document Control Desk Hashington 0.C. 20555 Docket No. 50-293 License No. DPR-35
Dear Sir:
The enclosed Licensee Event Report (LER) 89-033-00, " Automatic Closing of the Group 1 (one) Isolation Valves due to High Reactor Vessel Water Level During Startup", is submitted in accordance with 10 CFR Part 50.73.
Please do not hesitate to cor. tact me if there are any questions regarding this report.
G B DHE/bal
Enclosure:
LER 89-033-00 cc: Mr. Hilliam Russell Regional Administrator, Region I U.S. Nuclear Regulatory Commission 475 Allendale Rd.
King of Prussia, PA 19406 Sr. NRC Resident Inspector - Pilgrim Station Standard BECo LER Distribution 8912140406 891106 7'62 L
.PDR. ADOCK 05000293 f
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. LPPRIVED OMB EO 3100 0104 LICENSEE EVENT REPORT (LER) '" ma ' ' M '
F ACILITY NAME 111 PDCKET NUMBER Q) PAGE G Pilgrim Nuclear Power Station 1 loFl 0 f r; 0 l5 l 010 l 0121913
"' Automatic Closing of the Group 1 (one) Isolation Valves due to liigh Reactor Vessel l Water Level During Startup EVENT DATE ($1 LER TUMBER 461 REPORT DATE (7) OTHER F ActLITl!5 INVOLVED 48) ,
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NAME TELEPHONE NUMBER ARE A CODE Douglas W. Ellis - Senior Compliance Engineer 5 1018 7141 71-I8 11 1610 COMPL ETE ONE LINE FOR E ACH COMPONENT F AILURE DESCRIBED IN THIS REPORT H31 j M ' C' "I'0RTA LE MA RE TA E ,
CAUSE SYST EM COMPONENT 0 CAUSE S V E?t M COMPONENT FdC-1 l I I I l l 1 1 1 I i l I i l I I I I I I I I I I I I I SUPPLEMENT AL PEPORT EXPECTED M41 MONTH DAY YEAR 5 $iN 4t$ fl4 yet, empton IXPECTED $UMEIS$10Ar OA TEb NO l l l ASSTs.ACT ILimit to 1400 speces le , approntornatem sfwen e smere saece typewertsen koos) '16 >
l On November 6,1989 at 1539 hours0.0178 days <br />0.428 hours <br />0.00254 weeks <br />5.855895e-4 months <br />, an automatic actuation of the Group 1 (one)
I portion of the Primary Containment Isolation Control System (PCIS) occurred during l the initial stage of a startup. The actuation resulted in the automatic closing of the related Primary Containment System isolation valves that were in the open position.
L l The direct cause for the actuation was high Reactor Vessel (RV) water level. The I high RV water level (+50 inches narrow range level) occurred because a six inch manually operated valve, located in-parallel with the Feedwater System startup regulating valve, was in the incorrect (open) position at the time of the startup.
Corrective action taken included closing the manual valve, restoring the RV water l
1evel to normal, resetting the PCIS logic circuitry, and a walkdown of applicable systems that revealed no other mispositioned valves. Corrective actions planned include improving verbal communications and relabeling the identification tags for remote reach rods to include the identification number of the valve connected to the reach rod.
This event occurred during the startup mode with the reactor mode selector switch in the STARTUP position. The reactor power level was approximately one percent.
The RV pressure was approximately three psig with the RV water temperature at 220 degrees Fahrenheit. This report is submitted in accordance with 10 CFR 50.73(a)(2)(iv) and this event posed no threat to the public health and safety.
N, C Form 366 (9 83)
e NRC Poem JESA U E NUCLEMI ELEULATOAY CDMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION areRoveo ove No. 3 iso-oio.
F ACitiTV hAME 03 DOCKti NUMBE R (21 LIR NUMgtR ($1 PW m n *R "nW:' "*;*7%
Pilgrim fluclear Power Station 015 l 0 l 0 l 0121913.8 l9 -
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0 l0 01 2 oF 0 15 nxis .,.-r. mc w me.mn EVENT DESCRIPTION 4 On November 6, 1989 at 1539 hours0.0178 days <br />0.428 hours <br />0.00254 weeks <br />5.855895e-4 months <br />, an automatic actuation of the Main Steam ;
System / Group 1 (one) portion of the Primary Containment Isolation Control System i (PCIS) occurred due to a high Reactor Vessel (RV) water level. j The actuation resulted in the following designed responses. The inboard and j
~
outboard Primary Containment System (PCS)/ Main Steam Isolation Valves (MSIVs), in the open position, closed automatically. The inboard and outboard PCS/ Main Steam drain valves (M0-220-1 and -2), in the open position, closed automatically. The.
inboard and outboard PCS/ Sample System valves (AO-220-44 and -45), in the open position, closed automatically, j The high RV water level occurred during the initial stage of the startup while at step 36 of Attachment 1 (OPER-01, "Startup Checklist") of procedure 2.1.1 (Rev. 59), "Startup from Shutdown". At that point in the startup, a Feedwater System Train 'A' block valve (M0-3477) was opened in order to provide condensate to the feedwater startup regulating valve (FV-643). The control switch for the block valve (M0-3477) is a seal-in type, i.e. the valve opens fully (60 seconds) upon demand. After the control switch was moved to the OPEN position, and as the valve M0-3477 was opening, the RV water level began to increase even though the startup regulating valve (FV-643) was in the closed position. [After the event the manually operated valve HO-443, located in-parallel with valve FV-643, was found to be in the (incorrect) open position.] Meanwhile, the control switch for valve -
M0-3477 was moved to the CLOSE position when the valve reached the fully open position. However, the Condensate System pump that was in service provided a flowrate through valve M0-3477 (being closed but with a 60 second closing time) and six inch valve H0-443, that was sufficient to result in the high RV water level.
The high RV water level resulted in the PCIS actuation before valve M0-3477 attained the fully closed position.
The RV water level was restored to normal (i.e., +30 inches narrow range level) by the letdown of water to the Main Condenser via the Reactor Water Cleanup System.
The PCIS logic circuitry was reset on November 6,1989 at 1635 hours0.0189 days <br />0.454 hours <br />0.0027 weeks <br />6.221175e-4 months <br /> and the affected valves were reopened.
Failure and Malfunction Report 89-428 was written to document the actuation. The NRC Operations Center was notified in accordance with 10 CFR 50.72 on November 6, 1989 at 1825 hours0.0211 days <br />0.507 hours <br />0.00302 weeks <br />6.944125e-4 months <br />.
This event occurred during the startup mode with the reactor mode selector switch in the STARTUP position. The control rods were in a partially withdrawn position with the reactor power level at approximately 1 (one) percent. The RV pressure was approximately 3 (three) psig with the RV water temperature at 220 degrees Fahrenheit. One of the three Condensate System pumps was in service. The Feedwater System pumps were not in service. The Feedwater System Train 'A' and Train 'B' regulating valves (FV-642A and FV-642B) and startup regulating valve (FV-643) were in the closed position and not in service.
l l ""'"' __ _ _ _ __ __ _ _
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION mRovso ove No aao-om exnRes owns F AC6tITY NAML (U DOCKET NUMetR 426 Lin huMeERlll PAGE (36
"*" INsIn NysIn P11erim Nuclear Power Station 0 l5 l0 l 0 l 0 l2 l 913 @9 -
01313 -
0l0 0la oF g l r; TEXT y more esece e reewsW ese essitons/ NRC Form Js5Cs4171 CAUSE ,
The direct cause for the actuation was a high RV water level condition. The maximum RV water level that occurred was approximately +50 inches (narrow range level).
The cause for the high RV water level was the mistaken opening of valve H0-443 instead of a feedwater startup manual block valve (H0-444B) while shutdown for '
scheduled maintenance and testing. Contributing causes were verbal miscommunication and less than adequate information provided on identification tags for manual valve remote operators (i.e., reach rods).
'The feedwater startup manual block valves (H0-444A and H0-4448) are normally open and are remotely operated via reach rods (S-6-8 for H0-444A and S-6-9 for H0-4448). Valve HO-443 is normally closed and is also remotely operated via a reach rod (S-6-5). The label for each reach rod identifies the reach rod number (e.g., S-6-9) and functional description but does not specifically identify the '
valve (e.g., H0-444B) connected to the reach rod. During the outage, work was performed on the Feedwater System regulating valves (FV-642A and FV-6428) and the startup regulating valve (FV-643). After the work, the manual block valves (H0-444A and H0-444B) were to be opened. However, because of verbal
.miscommunication and less than adequate information (i.e., valve number not identified) on the identification tags for the reach rods, the feedwater startup bypass valve (H0-443) was opened instead of a feedwater startup block valve (H0-444B) when the block valves (H0-444A and H0-4448) were to be opened.
CORRECTIVE ACTION The-following corrective actions have been taken:
- The valve H0-443 was closed.
- The valve lineups for systems wd on during the outage were checked with satisfactory results. The ' m.up checks consisted of field inspection of specified valves in the Feedwater, High Pressure Coolant l
Injection, Reactor Core Isolation Cc'oling, Core Spray, and Residual Heat Removal Systems. The inspections revealed no other mispositioned valves.
Corrective actions planned include the following:
- Station Instruction SI-0P.006 (Rev.1), " Operations Communications", will
! be revised. The focus of the revision is to improve the specificity of l verbal instructions.
- The labeling of remote reach rods will be improved to include the identification of the valve on the reach rod identification label. The l
labeling is administratively controlled via procedure 1.3.79, " Operations Equipment Labeling".
l-g,o.. m. . - - .-_ _
NRC form.306A U $. NUCL112 K11ULATORY COMMI5810N
, LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Arenoveo oue =o 3 iso-oio4 J EXPIRES 5!31/98 j F ActLITV esaMt m DOCKil NUMSE R (2) L4R NUMSERISI PA06 (3)
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T1xt - 4.w mac-2.a4m SAFETY CONSEOUENCES This event posed no threat to the public health and safety.
The actuation was the designed response to the high RV water level. The water level that occurred, i.e. +50 inches narrow range level, was slightly above the high RV water level setpoint (calibrated at approximately +45 inches). The bottom of the 20 inch Main Steam System piping corresponds to a level approximately 112 inches above zero inches narrow range level. Therefore, the maximum RV water level that occurred (i.e., +50 inches) was approximately 62' inches below the Main Steam System piping.
This report is submitted in accordance with 10 CFR 50.73(a)(2)(iv) because the Group 1 (one) portion of the PCIS logic circuitry was actuated.
SIMILARITY TO PREVIOUS EVENTS A review was conducted of Pilgrim Station Licensee Event Reports (LERs) submitted since January 1984. The review focused on LERs submitted in accordance with 10 CFR 50.73(a)(2)(iv) that involved a high RV water level. The review identified high RV water level events that were reported in LERs 50-293/84-020-00, 85-014-00, 88-024-00, 89-007-00, and 89-015-00.
For LER 84-020-00, a PCIS Group 1 (one) isolation signal occurred due to a high RV water level on December 25, 1984 at 1905 hours0.022 days <br />0.529 hours <br />0.00315 weeks <br />7.248525e-4 months <br />. The isolation signal resulted in the automatic closing of the MSIVs. At the time of the event, the reactor power level was approximately one percent, the reactor mode selector switch (RMSS) was in the STARTUP position, the RV pressure was approximately 100 psig, the RV water level was being manually controlled, and the Residual Heat Removal System (RHRS) was in the Suppression Pool Cooling (SPC) mode of operation. The cause for the high water level was attributed to leakage of RHRS/SPC water past the seat of an RHRS valve (MO-1001-28A) and into the RV.
l For LER 85-014-00, a PCIS Group 1 (one) isolation signal and a Reactor Protection System (RPS) scram signal and reactor scram at 10 percent reactor power occurred due to a high RV water level on June 15, 1985 at 0435 hours0.00503 days <br />0.121 hours <br />7.19246e-4 weeks <br />1.655175e-4 months <br />. The isolation signal l resulted in the autoniatic closing of the MSIVs. At the time of the event, the RMSS i
was in the STARTUP position, the RV pressure was approximately 700 psig, and the RV water level was being manually controlled. The cause for the high water level was attributed to utility licensed operator error. The scram signal occurred because L
the RV pressure was approximately 700 psig when the HSIVs closed. A high water I level in the RV (i.e., closing of the MSIVs) results in a scram signal when the
- RMSS is in the REFUEL or SHUTDOWN or STARTUP position, and if the RV pressure is i
1 greater than approximately 600 psig.
l-l l
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.- LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Amovto ous wo. am-eio4 l
, EXPlRE 5: 8/31/88 F ACILITY NAest (H DOCEti NUMBER (21 ggg gygggg gg, pggg ggi "aa "=W l'#.7%
Pi1E; rim Nuclear Power Station- g, 9 9 _ _
TEXT f# moso eseco de mounoc( ese edweener 44C Form JW W 11h For LER 88-024-00, a PCIS Group 1 (one) isolation signal occurred due to a high RV water level on October 17, 1988 at 1433 hours0.0166 days <br />0.398 hours <br />0.00237 weeks <br />5.452565e-4 months <br />. The isolation signal resulted in the automatic closing of the MSIVs. At the time of the event, the reactor power level was zero percent, the RMSS was in the REFUEL position for a surveillance activity, the RV pressure was zero psig, and the RV water level was being manually controlled. The cause for the high water level was attributed to a pin that became disassociated from the feedback cam linkage of the positioner for the Feedwater System Train 'A' regulating valve (FV-642A).
For LER 89-007-00, a PCIS Group 1 (one) isolation signal occurred due to a high RV water level on February 4,1989 at 0936 hours0.0108 days <br />0.26 hours <br />0.00155 weeks <br />3.56148e-4 months <br />. The isolation signal resulted in the automatic closing of the inboard MSIVs. The outboard steam line 'C' MSIV closed automatically and the other outboard MSIVs remained closed. At the time of the event, the reactor power level was approximately 0.8 percent, the RMSS in the STARTUP position, and the RV pressure was approximately 278 psig. The MSIVs were being tested with a differential pressure of approximately 150 psid across the seat of the MSIV(s). The high water level was caused by the swell (expansion) of RV water that occurred when the outboard line 'C' MSIV was opened for testing. The cause for the event was attributed to an inadequacy in the development and review of the approved test procedure and a relatively fast opening time for the MSIV.
For LER 89-015-00, a high RV water level on May 3, 1989 at 0326 hours0.00377 days <br />0.0906 hours <br />5.390212e-4 weeks <br />1.24043e-4 months <br /> resulted in an automatic sequence of designed responses that included a Turbine-Generator Trip, a PCIS Group 1 (one) isolation signal, and an RPS scram signal ar.d reactor scram at 24 percent reactor power. At the time of the event, the RMSS was in the RUN position and the RV pressure was approximately 940 psig. The high water level occurred while troubleshooting the actuator controls for the Feedwater System Train
'B' regulating valve (FV-642B). The primary cause for the high water level was attributed to the use of a general troubleshooting procedure (3.M.3-8) for troubleshooting the actuator controls of the feedwater regulating valve (FV-6428).
ENERGY INDUSTRY IDENTIFICATION SYSTEM (EIIS) C00f3
~
The EIIS codes for this report are as follows:
l COMPONENTS CQQES Valve, Isolation ISV Valve, Control, Flow FCV SYSTEMS Condensate System SD Containment Isolation Control System (PCIS) JM Engineered Safety Features Actuation System (PCIS) JE Feedwater System SJ
! Main Steam System SB 1
l l
l g,o= =.. . ._ _ _ _ ._. ___ _ ___.