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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046C3131993-07-28028 July 1993 LER 93-015-00:on 930630,HPCI Sys Declared Inoperable Due to Indicated Flow During Surveillance.Caused by Foreign Matl That Plugged Portion of Restricting Orifice.Restricting Orifice Removed,Cleaned & reinstalled.W/930728 Ltr ML20046B5241993-07-26026 July 1993 LER 93-007-01:on 930317,automatic Closing of RCIC Sys Turbine Steam Supply Isolation Valves Occurred Due to High Steam Flow Signal.Increased Frequency of Valve Testing from Monthly to weekly.W/930726 Ltr ML20045F8601993-06-30030 June 1993 LER 93-014-00:on 930531,automatic Scram Occurred,Resulting from Operation of Auxiliary Transformer Differential Relay During Power Ascension.Uat Phase B & C Differential Relays Left Interchanged as Investigative aid.W/930630 Ltr ML20045E2301993-06-25025 June 1993 LER 93-013-00:on 930530,RCIC Sys Declared Inoperable & 7 Day TS 3.5.D.2 LCO Entered Due to Speed Oscillations Which Occurred After Several Minutes of steady-state Operation. Caused by Actuator Failure.Actuator replaced.W/930625 Ltr ML20045E2251993-06-25025 June 1993 LER 93-012-00:on 930529,unplanned PCIS Group I Isolation Signal Occurred While Opening MSIV During Startup,Resulting in Automatic Closing of Related Valves.Caused by Licensed Operator Error.Group 1 Isolation reset.W/930625 Ltr ML20045D6941993-06-23023 June 1993 LER 93-011-00:on 930525,determined That Initial as-found Popping Pressures of Pilot Valves for Three Target Rock Main Steam Relief Valves Out of TS Tolerance.Caused by Setpoint Drift.Valves Reworked & Reassembled by Target Rock Corp ML20045D1861993-06-18018 June 1993 LER 93-010-00:on 930519,SUT Became de-energized During Planned Calibr of Turbine/Generator Relays Lockout Test While Shut Down.Caused by Personnel Error.Discussion Conducted W/Personnel Re Attention to detail.W/930618 Ltr ML20044H0441993-06-0202 June 1993 LER 93-009-00:on 930504,circuit Breaker Did Not Close During Planned Bus Transfer Due to Loose Control Circuit Wire.Lug Replaced & Reterminated on 930505 & Post Work Testing Completed W/Satisfactory results.W/930602 Ltr ML20024G7451991-04-24024 April 1991 LER 91-005-00:on 910325,diesel Generator Inoperable,Causing Loss of Ac Power to Train B Components of Safety Sys & Actuating Portions of Primary/Secondary Containment Sys. Caused by Voltage Regulator failure.W/910424 Ltr ML20029A6721991-02-25025 February 1991 LER 91-001-00:on 910125,automatic Primary Containment Isolation Control Sys Group 5 Actuation Occurred,Resulting in Closing of RCIC Turbine Steam Supply Isolation Valves. Caused by High Flow conditions.W/910225 Ltr ML20028G9731990-09-20020 September 1990 LER 89-036-01:on 891122,determined That HPCI Sys Inoperable Due to Inoperable Gland Seal Condenser Blower Motor.Caused by age-related Wear of Motor.Blower Motor Replaced & Blower Tested W/Satisfactory results.W/900920 Ltr ML20028G9121990-09-18018 September 1990 LER 89-037-01:on 891130,primary Containment/Traversing in-core Probe Ball Valve Discovered to Be Almost Full Open. Caused by Damage to Valve Stem Due to Manual Manipulation of Stem.Ball Valve & Solenoid Actuator replaced.W/900918 Ltr ML20043G3541990-06-12012 June 1990 LER 90-008-00:on 900513,automatic Scram Resulting from Load Rejection Occurred While at Full Power,Resulting in Trip of Generator Field Breakers.Caused by Fault on Offsite 345 Kv Transmission sys.Loss-of-field Relay replaced.W/900612 Ltr ML20043F8291990-06-0606 June 1990 LER 90-007-00:on 900507,discovered That Drywell to Suppression Chamber Vacuum Breaker Surveillance Not Performed Prior to Startup in 1988.Caused by Misunderstanding of requirements.W/900606 Ltr ML20042F5911990-04-30030 April 1990 LER 90-006-00:on 900330,determined That Position of Primary Containment Sys Isolation Valve Not Recorded Daily,Per Tech Specs.Review Performed to Determine If Other Problems Existed.Plant Shut Down & Review performed.W/900430 Ltr ML20012F5751990-04-0606 April 1990 LER 90-003-00:on 900311,automatic Actuation of Main Steam Sys Group 1 Portion of Primary Containment Isolation Control Sys Occurred.Caused by False High Reactor Vessel Water Level Signal.Procedure Developed Re backfill.W/900406 Ltr ML20012E9831990-03-30030 March 1990 LER 90-002-00:on 900228,determined That Max Fraction of Limiting Power Density Not Checked Daily During Reactor Power Operation,Per Tech Spec 4.1.B.On 900323,addl Tech Spec Issue Discovered.Tech Specs changed.W/900330 Ltr ML20012C4871990-03-12012 March 1990 LER 90-001-00:on 900209,24 H Limiting Condition for Operation Entered When Two RCS Instrumentation Excess Flow Check Valves Inappropriately Verified Operable During Testing.Cause Undetermined.Two Valves replaced.W/900312 Ltr ML20005G0981990-01-0808 January 1990 LER 89-038-00:on 891208,unplanned Automatic Reactor Protection Sys Scram Signal & Reactor Scram Occurred.Caused by False Low Reactor Vessel Water Level Signal.Local Level Indicators Satisfactorily calibr.W/900108 Ltr ML20005F8481990-01-0808 January 1990 LER 89-039-00:on 891209,automatic Actuation of RHR Sys Portion of Primary Containment Isolation Control Sys Occurred.Caused by Hydrodynamic Transient That Actuated Protective High Pressure switches.W/900108 Ltr ML20005E8551989-12-30030 December 1989 LER 89-037-00:on 891130,discovered That Traversing in-core Probe Ball Valve,Mfg by Consolidated Controls,Inc,Closed,In Violation of Tech Specs.Caused by Damage to Valve Stem.Ball Valve & Actuator replaced.W/891230 Ltr ML20011D1361989-12-11011 December 1989 LER 89-035-00:on 891111,inadvertent Actuation of Portion of Secondary Containment Sys During Surveillance Testing Occurred.Caused by Location of Radiation Isolation Control Sys Channel a Logic Relay.Procedure revised.W/891211 Ltr ML20005D7421989-12-0606 December 1989 LER 89-033-00:on 891106,automatic Actuation of Group 1 Portion of Primary Containment Isolation Control Sys (PCIS) Occurred.Caused by High Reactor Vessel Water Level.Manual Valve Closed & PCIS Logic Circuitry reset.W/891206 Ltr ML19351A4581989-12-0606 December 1989 LER 89-034-00:on 891108,determined That Reactor Pressure Exceeded 150 Psig on 891107 W/O Performing Surveillance Procedure 8.5.4.4, HPCI Valve Operability Test. Caused by Personnel Error.Procedure initiated.W/891206 Ltr ML19332D1421989-11-22022 November 1989 LER 89-031-00:on 891024,closing Times for Two in-series Primary Containment Isolation Valves Exceeded Acceptance Criteria During Shutdown Testing.Cause Undetermined.Closing Time Retested W/Satisfactory results.W/891122 Ltr ML19332D6231989-11-20020 November 1989 LER 89-032-00:on 891020,pneumatic Pressure Drop for Two of Four Automatic Depressurization Sys Accumulators Discovered Greater than Max Acceptable Value.Caused by Leakage from Seat of Supply Check Valves.Seat replaced.W/891120 Ltr ML19324C3181989-11-0909 November 1989 LER 88-002-01:on 880117,full Reactor Protection Sys Scram Trip Signal Occurred During Surveillance Test,Resulting in Incomplete Actuations.Caused by Procedure Inadequacy.Logic Relay Replaced & Procedure revised.W/891109 Ltr ML19324B1131989-10-21021 October 1989 LER 89-030-00:on 890926,control Room High Efficiency Air Filtration Sys Flowrate non-conservative Due to Procedure Error.Caused by Transcription Error.Procedure Revised & Test Reperformed Using Corrected procedure.W/891021 Ltr ML19325D4681989-10-16016 October 1989 LER 89-029-00:on 890914,locked High Radiation Area Door Found to Have Been Unsecured Contrary to Tech Spec 6.13.2. Caused by Failure to Adhere to Approved Procedures. Training on Access Requirements initiated.W/891016 Ltr ML19325D1861989-10-10010 October 1989 LER 89-028-00:on 890907,HPCI Sys Declared Inoperable Because Mechanical Overspeed Trip Occurred During Surveillance Test. Caused by Failure of Ramp Generator Signal Converter Module. Module Removed & Sent to Mfg for exam.W/891010 Ltr ML17277B8221984-07-20020 July 1984 LER 82-049/01X-1:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting.Caused by Personnel Error.Valve Removed & Replaced W/Properly Set Spare Valve. Procedure revised.W/840720 Ltr ML20024C3231983-06-24024 June 1983 Updated LER 82-038/03X-1:on 820817,RCIC Steam Line High Differential Pressure Alarm Received.Caused by Air in Sensing Lines to Pressure Switches.Cross Threaded Cap Found on in-line Snubber.Snubber replaced.W/830624 Ltr ML20024C2211983-06-24024 June 1983 Updated LER 80-053/03X-1:on 800814,0907 & 14,HPCI Turbine Exhaust Line Snubber 23-3-36 Determined Inoperable.Caused by Transient Hydrodynamic Shock During Startup & Shutdown. Snubbers upgraded.W/830624 Ltr ML20024B8451983-06-24024 June 1983 LER 83-031/03L-0:on 830528,HPCI Sys Made Inoperable to Repair Steam Leak on AO 2301-31.Caused by Leaking Stem Packing.Packing Replaced.Valve Tested Satisfactorily.Sys Returned to svc.W/830624 Ltr ML20024B8321983-06-24024 June 1983 LER 83-030/03L-0:on 830527,both HPCI Area Smoke Detection Sys Alarmed in Main Control Room.Caused by Valve A02301-31 Steam Leak Causing False Indications.Valve repaired.W/830624 Ltr ML20024C3101983-06-21021 June 1983 Updated LER 79-007/03X-1:on 790212,while Performing Test 8.7.4.3,valves AO-5033A,CV-5065-10,15,16 & 17 Failed to Give Proper Position Indication When Cycled & to Close within Specified Tolerance.Cause Not stated.W/830621 Ltr ML20024A8861983-06-16016 June 1983 LER 83-027/03L-0:on 830518,during Routine Insp,Folding Fire Door Found Inoperable.Caused by Operating Cable Becoming Detached from Pulley Due to Slack.Cable Reattached & Operating Mechanism adjusted.W/830616 Ltr ML20023D1691983-05-0909 May 1983 Updated LER 82-008/01X-1:on 820331,HPCI Injection Valve MO-2301-8 Failed to Open in Required Manner.Caused by Missing Wire Jumper Intended to Bypass Motor Operator Torque Switch.Jumper Installed & Valve Tested Satisfactorily ML20023D0671983-05-0909 May 1983 LER 83-021/03L-0:on 830411,during Surveillance Test 8.7.4.3, Primary Containment Isolation Valve AO-5033B Failed to Meet 10-s Closing Time Requirements.Caused by Lubricant Infiltrating Solenoid Valve Components.Components Replaced ML20023D0181983-05-0404 May 1983 LER 83-022/03L-0:on 830413,overload on Valve Motor 1301-17 Resulted in Loss of High Pressure Core Cooling Backup Capability.Caused by Oxidation in Motor End Bell & Motor Brushes,Due to Humidity Caused by Leaking Valve Packing ML20028G1591983-01-28028 January 1983 LER 83-002/01T-0:on 830116,flow Ref off-normal Alarm Received.Average Power Range Monitor Flux Scram Trip Settings Affected.Cause Under Investigation.Flow Inputs Monitored & Amplifier B Recalibr ML20028F4121983-01-17017 January 1983 LER 83-002/01X-0:on 830116,while Clearing off-normal Alarm for Flow Comparators,Average Power Range Monitor Flux Scram Trip Settings Found in Nonconservative Direction.Caused by Drifting Proportional Amplifiers.Settings Checked Daily ML20028B0421982-11-16016 November 1982 LER 82-049/01T-0:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting of 1240 Psig, Exceeding Tech Specs.Caused by Personnel Error.Set Valve Removed,Procedure Adherence Stressed & Procedure Revised ML20027C9801982-10-20020 October 1982 LER 82-039/03L-0:on 820920,timing Tests of Three Reactor Water Cleanup Isolation Valves 1201-2,-5 & -80 Not Completed within Allowed Time.Caused by Operational Constraints Requiring Testing at Reduced Power ML20027C9941982-10-20020 October 1982 LER 82-040/03L-0:on 820920,found Reactor Protection Sys Initiation Function of Turbine Stop Valve Completed 1 Day Late.Caused by Decision to Defer Test Due to MSIV D Line Isolation.Tracking Sys Implemented to Prevent Recurrences ML20052B9141982-04-23023 April 1982 LER 82-010/03L-0:on 820326,during Review of Testing Requirements,Surveillance Test 8.I.4 Standby Liquid Control Sys Found Not Verified.Caused by Breakdown in Multidiscipline Review of Results ML20052F2071982-04-14014 April 1982 Updated LER 81-060/03X-1:on 811020,determined Potential Exists to Reduce Number of Operable APRM & IRM Instrument Channels in Rod Block Trip Sys to Below Tech Spec Min ML20050A6321982-03-19019 March 1982 Updated LER 82-055/01T-1:on 810926,during Shutdown,Yarway Level Indicators Started Oscillating.Drywell Temp Was 240 F at 81-ft W/Elevation Coolant Temp 220 F.Caused by Ineffective Drywell Cooling.Ventilation Returned to Svc ML20050A4521982-03-19019 March 1982 LER 82-006/01T-0:on 820304,while Performing Maint Re SIL 352 on Pressure Adjustment Mechanism HPCI Stop Valve,Three Broken cap-screws Found.No Cause Determined.Screws Examined, Replaced & Sys Returned to Svc ML20050A4331982-03-19019 March 1982 Updated LER 81-062/01X-1:on 811116,Wyle Labs Informed Util That Two Target Rock Safety Relief Valves Had Not Passed Setpoint Tests.Caused by Setpoint Shift Due to Changes to Designed Differential Forces from Excessive Pilot Leakage 1993-07-28
[Table view] Category:RO)
MONTHYEARML20046C3131993-07-28028 July 1993 LER 93-015-00:on 930630,HPCI Sys Declared Inoperable Due to Indicated Flow During Surveillance.Caused by Foreign Matl That Plugged Portion of Restricting Orifice.Restricting Orifice Removed,Cleaned & reinstalled.W/930728 Ltr ML20046B5241993-07-26026 July 1993 LER 93-007-01:on 930317,automatic Closing of RCIC Sys Turbine Steam Supply Isolation Valves Occurred Due to High Steam Flow Signal.Increased Frequency of Valve Testing from Monthly to weekly.W/930726 Ltr ML20045F8601993-06-30030 June 1993 LER 93-014-00:on 930531,automatic Scram Occurred,Resulting from Operation of Auxiliary Transformer Differential Relay During Power Ascension.Uat Phase B & C Differential Relays Left Interchanged as Investigative aid.W/930630 Ltr ML20045E2301993-06-25025 June 1993 LER 93-013-00:on 930530,RCIC Sys Declared Inoperable & 7 Day TS 3.5.D.2 LCO Entered Due to Speed Oscillations Which Occurred After Several Minutes of steady-state Operation. Caused by Actuator Failure.Actuator replaced.W/930625 Ltr ML20045E2251993-06-25025 June 1993 LER 93-012-00:on 930529,unplanned PCIS Group I Isolation Signal Occurred While Opening MSIV During Startup,Resulting in Automatic Closing of Related Valves.Caused by Licensed Operator Error.Group 1 Isolation reset.W/930625 Ltr ML20045D6941993-06-23023 June 1993 LER 93-011-00:on 930525,determined That Initial as-found Popping Pressures of Pilot Valves for Three Target Rock Main Steam Relief Valves Out of TS Tolerance.Caused by Setpoint Drift.Valves Reworked & Reassembled by Target Rock Corp ML20045D1861993-06-18018 June 1993 LER 93-010-00:on 930519,SUT Became de-energized During Planned Calibr of Turbine/Generator Relays Lockout Test While Shut Down.Caused by Personnel Error.Discussion Conducted W/Personnel Re Attention to detail.W/930618 Ltr ML20044H0441993-06-0202 June 1993 LER 93-009-00:on 930504,circuit Breaker Did Not Close During Planned Bus Transfer Due to Loose Control Circuit Wire.Lug Replaced & Reterminated on 930505 & Post Work Testing Completed W/Satisfactory results.W/930602 Ltr ML20024G7451991-04-24024 April 1991 LER 91-005-00:on 910325,diesel Generator Inoperable,Causing Loss of Ac Power to Train B Components of Safety Sys & Actuating Portions of Primary/Secondary Containment Sys. Caused by Voltage Regulator failure.W/910424 Ltr ML20029A6721991-02-25025 February 1991 LER 91-001-00:on 910125,automatic Primary Containment Isolation Control Sys Group 5 Actuation Occurred,Resulting in Closing of RCIC Turbine Steam Supply Isolation Valves. Caused by High Flow conditions.W/910225 Ltr ML20028G9731990-09-20020 September 1990 LER 89-036-01:on 891122,determined That HPCI Sys Inoperable Due to Inoperable Gland Seal Condenser Blower Motor.Caused by age-related Wear of Motor.Blower Motor Replaced & Blower Tested W/Satisfactory results.W/900920 Ltr ML20028G9121990-09-18018 September 1990 LER 89-037-01:on 891130,primary Containment/Traversing in-core Probe Ball Valve Discovered to Be Almost Full Open. Caused by Damage to Valve Stem Due to Manual Manipulation of Stem.Ball Valve & Solenoid Actuator replaced.W/900918 Ltr ML20043G3541990-06-12012 June 1990 LER 90-008-00:on 900513,automatic Scram Resulting from Load Rejection Occurred While at Full Power,Resulting in Trip of Generator Field Breakers.Caused by Fault on Offsite 345 Kv Transmission sys.Loss-of-field Relay replaced.W/900612 Ltr ML20043F8291990-06-0606 June 1990 LER 90-007-00:on 900507,discovered That Drywell to Suppression Chamber Vacuum Breaker Surveillance Not Performed Prior to Startup in 1988.Caused by Misunderstanding of requirements.W/900606 Ltr ML20042F5911990-04-30030 April 1990 LER 90-006-00:on 900330,determined That Position of Primary Containment Sys Isolation Valve Not Recorded Daily,Per Tech Specs.Review Performed to Determine If Other Problems Existed.Plant Shut Down & Review performed.W/900430 Ltr ML20012F5751990-04-0606 April 1990 LER 90-003-00:on 900311,automatic Actuation of Main Steam Sys Group 1 Portion of Primary Containment Isolation Control Sys Occurred.Caused by False High Reactor Vessel Water Level Signal.Procedure Developed Re backfill.W/900406 Ltr ML20012E9831990-03-30030 March 1990 LER 90-002-00:on 900228,determined That Max Fraction of Limiting Power Density Not Checked Daily During Reactor Power Operation,Per Tech Spec 4.1.B.On 900323,addl Tech Spec Issue Discovered.Tech Specs changed.W/900330 Ltr ML20012C4871990-03-12012 March 1990 LER 90-001-00:on 900209,24 H Limiting Condition for Operation Entered When Two RCS Instrumentation Excess Flow Check Valves Inappropriately Verified Operable During Testing.Cause Undetermined.Two Valves replaced.W/900312 Ltr ML20005G0981990-01-0808 January 1990 LER 89-038-00:on 891208,unplanned Automatic Reactor Protection Sys Scram Signal & Reactor Scram Occurred.Caused by False Low Reactor Vessel Water Level Signal.Local Level Indicators Satisfactorily calibr.W/900108 Ltr ML20005F8481990-01-0808 January 1990 LER 89-039-00:on 891209,automatic Actuation of RHR Sys Portion of Primary Containment Isolation Control Sys Occurred.Caused by Hydrodynamic Transient That Actuated Protective High Pressure switches.W/900108 Ltr ML20005E8551989-12-30030 December 1989 LER 89-037-00:on 891130,discovered That Traversing in-core Probe Ball Valve,Mfg by Consolidated Controls,Inc,Closed,In Violation of Tech Specs.Caused by Damage to Valve Stem.Ball Valve & Actuator replaced.W/891230 Ltr ML20011D1361989-12-11011 December 1989 LER 89-035-00:on 891111,inadvertent Actuation of Portion of Secondary Containment Sys During Surveillance Testing Occurred.Caused by Location of Radiation Isolation Control Sys Channel a Logic Relay.Procedure revised.W/891211 Ltr ML20005D7421989-12-0606 December 1989 LER 89-033-00:on 891106,automatic Actuation of Group 1 Portion of Primary Containment Isolation Control Sys (PCIS) Occurred.Caused by High Reactor Vessel Water Level.Manual Valve Closed & PCIS Logic Circuitry reset.W/891206 Ltr ML19351A4581989-12-0606 December 1989 LER 89-034-00:on 891108,determined That Reactor Pressure Exceeded 150 Psig on 891107 W/O Performing Surveillance Procedure 8.5.4.4, HPCI Valve Operability Test. Caused by Personnel Error.Procedure initiated.W/891206 Ltr ML19332D1421989-11-22022 November 1989 LER 89-031-00:on 891024,closing Times for Two in-series Primary Containment Isolation Valves Exceeded Acceptance Criteria During Shutdown Testing.Cause Undetermined.Closing Time Retested W/Satisfactory results.W/891122 Ltr ML19332D6231989-11-20020 November 1989 LER 89-032-00:on 891020,pneumatic Pressure Drop for Two of Four Automatic Depressurization Sys Accumulators Discovered Greater than Max Acceptable Value.Caused by Leakage from Seat of Supply Check Valves.Seat replaced.W/891120 Ltr ML19324C3181989-11-0909 November 1989 LER 88-002-01:on 880117,full Reactor Protection Sys Scram Trip Signal Occurred During Surveillance Test,Resulting in Incomplete Actuations.Caused by Procedure Inadequacy.Logic Relay Replaced & Procedure revised.W/891109 Ltr ML19324B1131989-10-21021 October 1989 LER 89-030-00:on 890926,control Room High Efficiency Air Filtration Sys Flowrate non-conservative Due to Procedure Error.Caused by Transcription Error.Procedure Revised & Test Reperformed Using Corrected procedure.W/891021 Ltr ML19325D4681989-10-16016 October 1989 LER 89-029-00:on 890914,locked High Radiation Area Door Found to Have Been Unsecured Contrary to Tech Spec 6.13.2. Caused by Failure to Adhere to Approved Procedures. Training on Access Requirements initiated.W/891016 Ltr ML19325D1861989-10-10010 October 1989 LER 89-028-00:on 890907,HPCI Sys Declared Inoperable Because Mechanical Overspeed Trip Occurred During Surveillance Test. Caused by Failure of Ramp Generator Signal Converter Module. Module Removed & Sent to Mfg for exam.W/891010 Ltr ML17277B8221984-07-20020 July 1984 LER 82-049/01X-1:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting.Caused by Personnel Error.Valve Removed & Replaced W/Properly Set Spare Valve. Procedure revised.W/840720 Ltr ML20024C3231983-06-24024 June 1983 Updated LER 82-038/03X-1:on 820817,RCIC Steam Line High Differential Pressure Alarm Received.Caused by Air in Sensing Lines to Pressure Switches.Cross Threaded Cap Found on in-line Snubber.Snubber replaced.W/830624 Ltr ML20024C2211983-06-24024 June 1983 Updated LER 80-053/03X-1:on 800814,0907 & 14,HPCI Turbine Exhaust Line Snubber 23-3-36 Determined Inoperable.Caused by Transient Hydrodynamic Shock During Startup & Shutdown. Snubbers upgraded.W/830624 Ltr ML20024B8451983-06-24024 June 1983 LER 83-031/03L-0:on 830528,HPCI Sys Made Inoperable to Repair Steam Leak on AO 2301-31.Caused by Leaking Stem Packing.Packing Replaced.Valve Tested Satisfactorily.Sys Returned to svc.W/830624 Ltr ML20024B8321983-06-24024 June 1983 LER 83-030/03L-0:on 830527,both HPCI Area Smoke Detection Sys Alarmed in Main Control Room.Caused by Valve A02301-31 Steam Leak Causing False Indications.Valve repaired.W/830624 Ltr ML20024C3101983-06-21021 June 1983 Updated LER 79-007/03X-1:on 790212,while Performing Test 8.7.4.3,valves AO-5033A,CV-5065-10,15,16 & 17 Failed to Give Proper Position Indication When Cycled & to Close within Specified Tolerance.Cause Not stated.W/830621 Ltr ML20024A8861983-06-16016 June 1983 LER 83-027/03L-0:on 830518,during Routine Insp,Folding Fire Door Found Inoperable.Caused by Operating Cable Becoming Detached from Pulley Due to Slack.Cable Reattached & Operating Mechanism adjusted.W/830616 Ltr ML20023D1691983-05-0909 May 1983 Updated LER 82-008/01X-1:on 820331,HPCI Injection Valve MO-2301-8 Failed to Open in Required Manner.Caused by Missing Wire Jumper Intended to Bypass Motor Operator Torque Switch.Jumper Installed & Valve Tested Satisfactorily ML20023D0671983-05-0909 May 1983 LER 83-021/03L-0:on 830411,during Surveillance Test 8.7.4.3, Primary Containment Isolation Valve AO-5033B Failed to Meet 10-s Closing Time Requirements.Caused by Lubricant Infiltrating Solenoid Valve Components.Components Replaced ML20023D0181983-05-0404 May 1983 LER 83-022/03L-0:on 830413,overload on Valve Motor 1301-17 Resulted in Loss of High Pressure Core Cooling Backup Capability.Caused by Oxidation in Motor End Bell & Motor Brushes,Due to Humidity Caused by Leaking Valve Packing ML20028G1591983-01-28028 January 1983 LER 83-002/01T-0:on 830116,flow Ref off-normal Alarm Received.Average Power Range Monitor Flux Scram Trip Settings Affected.Cause Under Investigation.Flow Inputs Monitored & Amplifier B Recalibr ML20028F4121983-01-17017 January 1983 LER 83-002/01X-0:on 830116,while Clearing off-normal Alarm for Flow Comparators,Average Power Range Monitor Flux Scram Trip Settings Found in Nonconservative Direction.Caused by Drifting Proportional Amplifiers.Settings Checked Daily ML20028B0421982-11-16016 November 1982 LER 82-049/01T-0:on 821102,main Steam Line Safety Valve a Set W/Nitrogen at Steam Relief Setting of 1240 Psig, Exceeding Tech Specs.Caused by Personnel Error.Set Valve Removed,Procedure Adherence Stressed & Procedure Revised ML20027C9801982-10-20020 October 1982 LER 82-039/03L-0:on 820920,timing Tests of Three Reactor Water Cleanup Isolation Valves 1201-2,-5 & -80 Not Completed within Allowed Time.Caused by Operational Constraints Requiring Testing at Reduced Power ML20027C9941982-10-20020 October 1982 LER 82-040/03L-0:on 820920,found Reactor Protection Sys Initiation Function of Turbine Stop Valve Completed 1 Day Late.Caused by Decision to Defer Test Due to MSIV D Line Isolation.Tracking Sys Implemented to Prevent Recurrences ML20052B9141982-04-23023 April 1982 LER 82-010/03L-0:on 820326,during Review of Testing Requirements,Surveillance Test 8.I.4 Standby Liquid Control Sys Found Not Verified.Caused by Breakdown in Multidiscipline Review of Results ML20052F2071982-04-14014 April 1982 Updated LER 81-060/03X-1:on 811020,determined Potential Exists to Reduce Number of Operable APRM & IRM Instrument Channels in Rod Block Trip Sys to Below Tech Spec Min ML20050A6321982-03-19019 March 1982 Updated LER 82-055/01T-1:on 810926,during Shutdown,Yarway Level Indicators Started Oscillating.Drywell Temp Was 240 F at 81-ft W/Elevation Coolant Temp 220 F.Caused by Ineffective Drywell Cooling.Ventilation Returned to Svc ML20050A4521982-03-19019 March 1982 LER 82-006/01T-0:on 820304,while Performing Maint Re SIL 352 on Pressure Adjustment Mechanism HPCI Stop Valve,Three Broken cap-screws Found.No Cause Determined.Screws Examined, Replaced & Sys Returned to Svc ML20050A4331982-03-19019 March 1982 Updated LER 81-062/01X-1:on 811116,Wyle Labs Informed Util That Two Target Rock Safety Relief Valves Had Not Passed Setpoint Tests.Caused by Setpoint Shift Due to Changes to Designed Differential Forces from Excessive Pilot Leakage 1993-07-28
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217E3021999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Pilgrim Nuclear Station.With ML20212C2921999-09-16016 September 1999 SER Accepting Licensee Request for Relief from ASME Code Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Pilgrim Nuclear Power Station ML20216F3511999-09-0808 September 1999 ISI Summary Rept for Refuel Outage 12 at Pnps ML20216E6881999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pilgrim Nuclear Power Station.With ML20210R3401999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Pilgrim Nuclear Power Station.With ML20209C4731999-07-0707 July 1999 Addendum to SE on Proposed Transfer of Operating License & Matls License from Boston Edison Co to Entergy Nuclear Generation Co ML20209H8251999-07-0101 July 1999 Provides Commission with Evaluation of & Recommendations for Improvement in Processes Used in Staff Review & Approval of Applications for Transfer of Operating Licenses of TMI-1 & Pilgrim Station ML20209E6191999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Pilgrim Nuclear Power Station.With ML20196H2451999-06-29029 June 1999 SER Denying Licensee Proposed Alternative in Relief Request PRR-13,rev 2.Staff Determined That Proposed Alternative Provides Insufficient Info to Determine Adequacy of Scope of Implementation ML20209A8901999-06-28028 June 1999 SER Accepting Licensee Proposed Alternative to Use Code Case N-573 for Remainder of 10-year Interval Pursuant to 10CFR50.55a(a)(3)(i) ML20209B9861999-06-23023 June 1999 Rev 13A to Pilgrim Nuclear Power Station COLR for Cycle 13 ML20217N9061999-06-21021 June 1999 Rept of Changes,Tests & Experiments for Period of 970422-990621 ML20195K3431999-06-15015 June 1999 Safety Evaluation Granting Licensee Request to Use Guidance of GL 90-05 to Repair Flaws in ASME Class 3 Salt Svc Water System Piping for Plant ML20195G8231999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Pnps.With ML20207E7471999-05-27027 May 1999 Safety Evaluation Granting Request Re Reduction of IGSCC Insp of Category D Welds Due to Implementation of HWC to License DPR-35 ML20206M1971999-05-11011 May 1999 SER Accepting Request for Approval to Repair Flaws in ASME Code Class 3 Salt Svc Water Piping at Plant ML20206J6611999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Pilgrim Nuclear Power Station.With ML20205L0221999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Pilgrim Nuclear Power Station.With ML20207J5471999-03-0909 March 1999 Training Simulator,1999 4-Yr Certification Rept ML20207F9401999-03-0101 March 1999 Long Term Program Semi-Annual Rept for Pilgrim Nuclear Power Station ML20207H5451999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Pilgrim Nuclear Power Station.With ML20196E2151998-12-31031 December 1998 1998 Annual Rept for Boston Edison & Securities & Exchange Commission Form 10-K Rept.With ML20206Q2741998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Pilgrim Nuclear Power Station.With ML20197J3591998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Pilgrim Nuclear Power Station.With ML20195C9951998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Pilgrim Nuclear Power Station.With ML20154K0721998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Pilgrim Nuclear Power Station.With ML20153D3901998-09-22022 September 1998 Safety Evaluation Granting 970707 Request to Use Guidance in GL 90-05 to Repair Flaws in ASME Class 3 Salt Svc Water Sys Piping for Pilgrim Nuclear Power Station ML20197C5011998-09-0404 September 1998 Rev 12C,Pages 4 & 5 to Pilgrim Nuclear Power Station Colr ML20197C5471998-08-31031 August 1998 Rev 12C to Pilgrim Nuclear Power Station Colr ML20151W8231998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Pilgrim Nuclear Power Station.With ML20237E2251998-08-26026 August 1998 Suppl & Revs to SE for Amend 173 for Pigrim Nuclear Power Station ML20237A9941998-07-31031 July 1998 Monthly Operating Rept for Pilgrim Nuclear Power Station ML20236U8201998-07-13013 July 1998 Rev 12B to Pilgrim Nuclear Power Station COLR (Cycle 12) ML20236P0151998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Pilgrim Nuclear Power Station ML20249A3741998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Pilgrim Nuclear Power Station.W/Undated Ltr ML20247H2081998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Pilgrim Nuclear Power Station ML20207B7601998-03-31031 March 1998 Final Rept, Pilgrim Nuclear Power Station Site-Specific Offsite Radiological Emergency Preparedenss Prompt Alert & Notification System Quality Assurance Verification, Prepared for FEMA ML20216G3911998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Pilgrim Nuclear Power Station ML20216J3741998-03-19019 March 1998 Safety Evaluation Accepting Licensee Request to Evaluate Elevated Tailpipe Temp on Safety Relief Valve SRV 203-3B ML20248L2241998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Pilgrim Nuclear Station ML20202G5251998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Pilgrim Nuclear Power Station ML20236M8511997-12-31031 December 1997 1997 Annual Rept for Boston Edison & Securities & Exchange Commission Form 10-K Rept ML20198L7701997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Pilgrim Nuclear Power Station ML20203D6101997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Pilgrim Nuclear Power Station ML20202D5761997-11-0808 November 1997 1997 Evaluated Exercise BECO-LTR-97-111, Monthly Operating Rept for Oct 1997 for Pilgrim Nuclear Power Station1997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Pilgrim Nuclear Power Station ML20217D6431997-10-0101 October 1997 Safety Evaluation Granting Request for Approval to Repair Flaws in Accordance W/Gl 90-05 for ASME Class 3 SSW Piping for Pilgrim ML20217H5621997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Pilgrim Nuclear Power Station ML20216J4131997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Pilgrim Nuclear Power Station ML20210J3321997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Pilgrim Nuclear Power Station 1999-09-08
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- [j 10 CFR 50.73 BOSTON EDISCN Pilgrim Nuclear Power Station Rocky Hdi Road Plymouth, Massachusetts 02360 July 26,1993 BECo Ltr. 93- 093
=
E. T. Boulette, PhD 3enior Vice President-Nuclear f U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C. 20555 '
Docket No. 50-293 j g License No. DPR-35 g SI The enclosed supplemental Licensee Event Report (LER) 93-007-01, " Automatic Closing B-of the RCIC System Turbine Steam Supply Isolation Valves due to High Steam Flow Signal", is submitted in accordance with 10 CFR Part 50.73.
Please do not hesitate to contact me if there are any questions regarding this report.
b (b E. T. Boulette, PhD RLC/bal
Enclosure:
Supplemental LER 93-007-01 cc: Mr. Thomas T. Martin Regional Administrator, Region I y U.S. Nuclear Regulatory Commission i 475 Allendale Rd.
King of Prussia, PA 19403 Mr. R. B. Eaton Div. of Reactor Projects I/II Office of NRR - USNRC One White Flint North - Mail Stop 14D1 11E55 Rockville Pike hockville, MD 20852 Sr. NRC Resident Inspector - Pilgrim Station Standard BEco LER Distrjhution bM
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NRC FORM 36[ U.S. NUCLEAR REGULAVORY COMMISSION APPROtfED BV OMB MO. 3150-0104 u,. m , EXPIRES 5/31/95 ESTIMATED BURDEN PER RE SPONSE TO COMPLY WrTN THIS
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CC C ""y "O M' r o r Us1 s I1Cs o nao r iL.C e m) 51 COMMENTS REGARDING BURDEN ES?iMATE TO THE INFORMATtDN AND RECORDS MANAGEMENT BRANCH IMNBB 7 714;. U.S. NUCLEAR REGJLATORY COMM!S$1GN, WA$ettN3 TON, DC /C%5.CCOL AND TO THE FAPERWORK REDUCTtON PRCUECT m5401% 03 FACE (5ee reverse foe number c8 dgNcharacters for each b6ccm) Or MANAGEMENT AND BUDGET,'tARH!N37CA DC 20503 FACILITY NAME (1) DCCKET NUMBER (2) PAGE (3)
PlLGRIM NUCLEAR POWER STATION 05000 -293 1 of 6 TITLE (4)
Automatic Closing of the RCIC System Turbine Steam Supply isolation Valves due to High Steam Flow Signal EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
SEQUENT,AL REitSION F ACluTY NAME DOCKET NJMBER MONN DAY YEAR YEAR NUMBE R NUMBER MONTH DAY YEAR N/A 05000 F ACILrrY NAVE [KOET NUMBE R 03 17 93 93 007 01 07 26 93 N/A 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 6: (Check one or more)(11)
ODE p) N X 50.73(aH2>0v) 20.402(b) 20 405fe) 73.71(b)
P R 20.405(a)(110) 50.36(cH1) X 50 73(a)(2Hv) (D) 73.71(c)
LE O) 002 l 20.405(a)(1)Gi) 50.36(c)(2) 50 73(a)(2Hvii) OTHER 20.405(a)(1)6ii) 50.73(aH210) 50.73(a)(2Hviii)(A) 20 405(a)(1) liv) 50.73(a)(2Mii) 50.73(aH2)(viii)(B) Agt;gtg 20.405(a)(1)(v) 50.73(aH2)0ii) 50.73(a)(2)(x) rom. 3%AJ LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER pocbde Area Code)
Robert L Cannon - Senior. Compliance Engineer (508) 747-8321 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSEM COMPONENT MANUF ACTURER S CAUSE SYL cM COMPONENT MANUFACTURER R A BN 20 L200 Yes SUPPLEMENTAL REPORT EXPECTED (14) "" * **
EXPECTED YES NO SUBMISSION I" Y** comp'*e EXPECTED SUBMISSION DA'E)
DATE (15)
[
X 3 3 TRACT (Limit to 1400 spaces, i e., approximately *s smgle-spM typewnten knes)(16)
On March 17, 1993, at 0024 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, an automatic Primary Containment Isolation Control System (PCIS) Group 5 actuation occurred while attempting to place the Reactor Core Isolation Cooling (RCIC) System in standby service durmg the performance of Procedure 2.1.1, "Startup from Shutdown". The actuation resulted in the closing of the RCIC turbine steam supply isolation valves M0-1301-16 and -17.
The isolation resulted from a high steam flow isolation signal while attempting to jog open the RCIC turbine steam supply valve M0-1301-16. After several attempts, valve MO-1301-16 was opened. The opening of the valve resulted in a rapid steam line pressurization and actuation of the steam flow sensors upstream of valve M0-1301-16. The inability to open MD-1301-16 on initial attempts was caused by a missing jumper that bypasses tne torque switch in the opening circuit. The missing jumper was installed and M0-1301-16 was satisfactorily tested.
This event occurred during plant startup while at 2 percent reactor power. The reactor mode selector switch was in STARTUP position. The Reactor Vessel (RV) pressure was 130 psig with RV temperature at approximately 360 degrees Fahrenheit. This report is submitted in accordance with 10 CFR 50.73 subpart (a)(2)(iv) and (a)(2)(v)(D). This event posed no threat to public health and safety.
N9C FORM 366A (M12)
NRC F RM 366A ' U.S. NUCLEAR REGULATORY COMMiss10N APPROVEo BY OMB NO. 3150-0104 n-m EXP!RES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WfrH THIS LICENSEE EVENT REPORT (LER) sl?EZ%%"3"JMOX0%"J " '
M TEXT CONTINUATION ^$E"NEsEENGToNIDcN$oN R u-TO THE PAPERWORK REDUCTION PRalECT (3140'041, OFFICE OF MANAGEMt NT AND BUDGET, WASMNGTON. DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) vtAR *EIP "O$$"R 2 of 6 PILGRIM NUCLEAR POWER STATION 05000-293 93 --007- 01 !
TEXT (tt more space is required, use additional copies of NRC Form 366A)(17) i REASON FOR SUPPLEMENT This supplement updates our root cause and corrective actions as described in our initial report. .
BACKGROUND The Reactor Core Isolation Cooling (RCIC) System turbine steam supply piping is equipped with differential pressure sensors (DPIS 1360-1A and -1B) that provide a steam line break detection function. A high steam flow signal in one or both logic channels functions to .
close the RCIC turbine steam supply piping isolation valves to limit the release of steam -
if a break in the RCIC turbine steam supply piping occurs. The Group 5 portion of the Primary Containment Irlation Control System (PCIS) controls the RCIC turbine steam supply valves (M0-1301-16 and -17) which close on the isolation signal.
EVENT DESCRIPTION On March 17,1993, at 0024 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, an unplanned automatic actuation of the RCIC portion of the PCIS occurred during the performance of Procedure 2.1.1, "Startup from Shutdown".
A startup from cold shutdown was in progress per Procedure 2.1.1. The operating supervisor'was on step 41 of Attachment 1 and instructed the operator to place RCIC into automatic standby mode in accordance with PNPS 2.2.22 (Rev. 39), " Reactor Core Isolation Cooling System", Attachment 7. The operator completed step 1 through 3 and was attempting to jog open M0-1301-16. The sequence consists of the following steps:
- 1. Verify inboard and outboard isolation valves M0-1301-16 and 1301-17 are shut.
- 2. Fully open outboard isolation valve M0-1301-17.
- 3. Crack open inboard isolation valve M0-1301-16.
- 4. Observe RCIC steam line pressure slowly increase to reactor pressure.
- 5. Fully open M0-1301-16.
As steps 1 through 3 were performed no increase in RCIC steam line pressure was observed.
The MD-1301-16 valve control switch was then taken to the closed position and this sequence was repeated a number of times in an attempt to pressurize the RCIC steam supply line. During a normal pressurization of the RCIC piping, the M0-1301-16 valve only needs to be cracked off its seat. A full stroke of this valve is approximately 8 seconds.
During each attempt to open the valve, the control switch was held in the open position slightly longer than the previous attempt, with no increase in downstream pressure. When the valve finally opened, it opened further than desired because of the time the control switch was held in the open position. The opening of the valve resulted in'a rapid steam line pressurization and actuation of the steam flow sensors upstream of valve M0-1301-16.
NRC FORM 300A 15 92)
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NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104
< s-m EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THS
' LICENSEE EVENT REPORT (LER) L" M' "RcRDfG lurJEi sCJ"OL%%% i TEXT CONTINUATION Su"ERY ccEs'MENofNE$o"$NS TO THE FAPERWOF4K REDUCTION PROJECT (31sts0104), OrF4CE OF MANAGEMLNT AND BUDGET, WASHINGTON, DC /
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR BR M 3 of 6 PILGRIM NUCLEAR POWER STATION 05000-293 93 --007- 01 TEXT (if more space is required, use add;tional copies of NRC Form 366A)(17)
M0-1301-16 is a jog valve in the open direction and is normally in the full open position.
MO-1301-16 h;s red and green indicating lights for valve position. Once the valve is ;
throttled (red and green indicating lights), there is no positive means to determine the actual valve position until the valve travels full open. The controls and indication for M0-1301-16 are located in the Control Room on Panel C-904. The RCIC turbine steam inlet pressure is displayed on PI-1340-6 and taps off the RCIC turbine steam piping, down stream of the valve MO-1301-17. :
Problem Report 93.9094 was written to document this event. The NRC Operations Center was notified in accordance with 10 CFR 50.72 at 0105 hours0.00122 days <br />0.0292 hours <br />1.736111e-4 weeks <br />3.99525e-5 months <br /> on March 17, 1993. i This event occurred during plant startup while at 2 percent reactor power. The reactor mode switch was in the STARTUP position. The Reactor Vessel pressure was 130 psig with RV ,
temperature at approximately 360 degrees Fahrenheit.
CAUSE !
A Failure Analysis Team (FAT) was established to assist in the collection and review of data regarding the inability of valve M0-1301-16 to initially open on March 16, 1993.
Following review and evaluation of the collected data, several possible causes were evaluated. Based on evaluation of the possible causes, none were considered credible except for possible intermittent operation of the torque switch bypass circuitry which is part of the valve's opening circuitry. Further investigation of the possible cause was ,
scheduled to be conducted during RF0 9.
Subsequent investigation during RF0 9 determined the electrical jumper that bypasses the torque switch in the valve's opening circuit was not installed. Problem Report 93.9213 ;
was written to document the discovery. The missing jumper was the reason valve MD-1301-16 ;
did not open on the initial attempts to open the valve.
During mid-cycle Outage (MCO) 9, MD-1301-16 was overhauled per Maintenance Request (MR) 19203092. To accomplish the overhaul, the actuator was removed from the Drywell to the. '
MOV refurbishment area in the Reactor Building. During the removal, the limit switch housing internals for M0-1301-16 were lost / misplaced. Replacement parts were withdrawn from the warehouse and the valve operator was to have been rewired in accordance with drawing M102B52, " Wiring Diagram Limitorque Motor Operator MD-1301-16". Drawing M102B52 does not show the presence of a jumper in the " standard way" Electrical Maintenance was accustomed. The torque switch bypass jumper was shown installed at the terminal strip rather than installed directly across the contacts of limit switch LS5. Although the correct configuration is also shown on drawing E5016 and MIG 15-9, the jumper was inadvertently ommitted when rewiring was performed during MCO 9. Failure to install the jumper is considered a maintenance preventable functional failure and is attributed to utility non-licensed Electrical Maintenance personnel error resulting from a lack of attention to detail. Also, contributing to the error is the non-standard manner in which this particular torque switch was bypassed and shown on drawing M102B52.
NRC FORM 366A 5 92)
1 NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-o104 t s-m EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WrrH THis LICENSEE EVENT REPORT (LER) L"2""' M G %'f "n# # % # L O NrT O 's TEXT CONTINUATION $5u"E*Es's"E'EsING [E[No"$N TO THE PAPETtWORK REDUCTON PROJECT (31500104). OFFICE OF MANAGEMENT AND RUDGET, WASHINGTON,DC 20503 FACILITY NAME (1) oOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR W 4 Of 6 j PILGRIM NUCLEAR POWER STATION 05000-293 93 --007- 01 TEMT (If more space is required, use additional copies of NRC Form 366A)(17)
CORRECTIVE ACTIONS Following the event, valve MD-1301-16 was operated several times and tested in accordance i with procedure 8.5.5.4, "RCIC Motor Operated Valve Operability Test Monthly / Quarterly".
No further abnormal operation was identified.
The frequency of valve M0-1301-16 testing was increased from monthly to weekly during the interval of March 17, 1993, to April 3, 1993 (beginning of Rf0 9).
During RF0 9 the missing electrical jumper was installed (MR19301054) and M0-1301-16 was satisfactorily tested.
Subsequent to installation of the electrical jumper in RF0 9, a review of the completed work determined the jumper had not been installed as shown on drawing M102B52. At the time of jumper installation, drawing M102B52 was reviewed by maintenance personnel and was mistakenly determined to be incorrect in that the drawing did not show the presence of a jumper in the " standard way" Electrical Maintenance was accustomed.
Electrical Maintenance personnel installed the jumper directly across the contacts of limit switch LS5 (" standard way") using schematic diagram E5016, rather than across termination points 3G and llF (electrically equivalent) on the termination strip as shown on drawing M102B52. Although the valve functions properly, the jumper is not installed in accordance with controlled drawing M102852. Problem Report 93.9320 was written to document this condition. Subsequent review by Operations and Engineering determined the operability of M0-1301-16 was not affected. Drawing M102B52 will be revised to reflect the as-wired configuration. This is considered an isolated occurrence. A review of the Problem Report database for similar wiring discrepancies did not identify a trend. A review of Problem Report 93.9213 was conducted with involved personnel, stressing the use of wiring diagrams rather than schematics when available. The Maintenance Section Manager will review this event with Maintenance Section personnel emphasizing the importance of attention to detail when conducting Maintenance activities.
SAFETY CONSE0VENCES This event posed no threat to the public health and safety.
The RCIC high steam flow isolation is designed to mitigate the consequences of a break in the RCIC turbine steam supply piping. The automatic closing of the RCIC turbine steam supply isolation valves prevents excessive loss of reactor coolant and the release of radioactive materials from the nuclear system process barrier if a break occurs. For this event, no break in the RCIC turbine steam line occurred.
Technical Specification 3.5.D.1 requires the RCIC System to be operable when reactor pressure is above 150 psig and temperature is above 360 degrees Fahrenheit. At the time of this event, the RCIC System was not required to be operable.
NHC f ORM 306A (5-921
NRC FORM 366A u.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 is.m EXPlRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS
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LICENSEE EVENT REPORT (LER) 1"0"s"nEMS'BTR2 M ELJ OMRTT2 TEXT CONTINUATION EUN NS ON G 2 0 10 TO THE PAPERWORK REDUCTON PRCUECT [31600104), OFFICE ,
OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503 FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR W MB R 5 of 6 PILGRIM NUCLEAR POWER STATION 05000-293 93 --007-- 01 TEXT (tf more space as required, use addttional copies of NRC Form 366A)(17)
M0-1301-16 is normally open when RCIC is required to be operable. The safety function of M0-1301-16 is to close upon a Group 5 isolation signal. The ability of M0-1301-16 to close was not affected by the missing jumper.
The Core Standby Cooling Systems (CSCS) consists of the High Pressure Coolant Injection (HPCI) System, Automatic Depressurization System (ADS), Core Spray System, and Residual Heat Removal (RHR) System / Low Pressure Coolant Injection (LPCI) mode. Although not part of the CSCS, the RCIC System is capable of providing water to the RV for high pressure '
core cooling, similar to the HPCI System. In the event the RCIC System were to become inoperable when its operation was necessary, operation of the HPCI System would provide water to the RV for high pressure core cooling. In the unlikely event the RCIC System were to become inoperable and the HPCI System was or were to become inoperable and high pressure core cooling was necessary, automatic (or manual) actuation of the ADS would depressurize the RV for low pressure core cooling provided independently by the Core Spray System and RHR/LPCI mode.
This report is submitted in accordance with 10 CFR 50.73(a)(2)(iv) because the closing of valves M0-1301-16 and -17 was not a planned part of the performance of Procedure 2.1.1 This report is also submitted in accordance with subpart (a)(2)(v)(D) because M0-1301-16, although normally in the open position, may not have opened automatically if an automatic -
initiation signal had occurred with the valve in the closed position.
SIMILARITY TO PREVIOUS EVENTS A review was conducted of Pilgrim Station Licensee Event Reports (LERs) submitted since January 1984. The review was focused on LERs submitted in accordance with 10 CFR 50.73(a)(2)(iv) involving a similar RCIC isolation due to high steam flow signals or 10 CFR 50.73(a)(2)(v)(D) involving similar improper wiring of MOVs. The review identified '
LFR 91-001-00.
For LER 91-001-00, on January 25, 1991, at 0956 hours0.0111 days <br />0.266 hours <br />0.00158 weeks <br />3.63758e-4 months <br /> and at 1407 hours0.0163 days <br />0.391 hours <br />0.00233 weeks <br />5.353635e-4 months <br />, an automatic !
closing of valves M0-1301-16 and -17 occurred during a surveillance test. The cause was a !
sensed RCIC turbine steam supply line high flow condition. The high steam flow condition occurred due to a failed transistor in the system's turbine speed control electric governor (EG-M). An exact cause of the transistor failure could not be identified.
However, the signal cable connecting the EG-M to the turbine control valve hydraulic actuator (EG-R) was found to be degraded. This degradation could have led to the transistor failure. The transistor and cable were replaced.
4 NRC FORM 366A &92)
9JRC FORM '}66A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 t s.m EXPIRES 5/31/95 ESTtMATED BURDEN PER Ff SPONSE TO COMPLY WrrH THIS LICENSEE EVENT REPORT (LER) EE",^J"REa"#S'Eu'Rinr*iMJ '
0,N4%fr*2 AND RFCORDS MANAGEMENT BRANCH (MNBB 7714). U.S. NUCLEAR TE.XT CONTINUATION nEeut4 Tony COMuissm. wAsHiNoTON. oC 205ss.oc,, ANo TO THE F'APERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGE MENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR R UMB 6 Of 6 PILGRIM NUCLEAR POWER STATION 05000-293 93 --007- g 01 TEXT (if more space is required, use additional coptes of NRC Form 366A)(17)
ENERGY INDUSTRY IDENTIFICATION (EIIS) CODES COMPONENTS CODES Valve, Electrically Operated 20 SYSTEMS Engineered Safety Features Actuation System (PCIS) JE Reactor Core Isolation Cooling System BN l
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