ML20039C525

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LER 81-114/03L-0:on 811121,B Loop of Rhr,Lpci Injection Valve 2E11-F015B,motor Breaker Tripped & Could Not Be Reset. Caused by Motor Windings Drawing Excessive Current Causing Windings to Deteriorate.Motor Replaced
ML20039C525
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 12/17/1981
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20039C516 List:
References
LER-81-114-03L, LER-81-114-3L, NUDOCS 8112290434
Download: ML20039C525 (2)


Text

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' 60 6' OOCAET % vgEm EVENT csscRIPTioN AND PROS ABLE CONSEQUENCES h "R" f_ con i 10 10! ! On November 21. 1981. with the unit 11 reactor at full cower. the I

of RHR, LPCI Injection Valve, 2E11-F015B, motor breaker tricoed and could total l I

not be reset. The "C" Loop of RHR was declared inoo and Tech Soec Section lo t Al l 3.5.3.2 was implemented. Redundant systems were operable. There were 1 lo is t 1 This is a i 10 !s l 1 no effects upon public health and safety due to this event.

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The motor breaker for "B" 1000 of RHR Injection Valve tripoed because 1

}inoil li!1 ji the motor windinas drew excessive current causina them to deteriorate.

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The motor was replace d and the injection valve proven operable and the t i ,

93; l "B" loop of RHR was returned to an operable status. ]

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e LER "o.: 50-366/1981-114 Licensee: Georgia Power Company Facility: Edwin I. Hatch Docket No.: 50-366 Narrative Report for LER 50-366/1981-114 On November 21, 1981, with the Unit II reactor operating at full power (995), the "B" loop RHR Injection Valve, 2E11-F015B, motor breaker tripped and would not reset. An investigation revealed valve, 2E11-F015B, motor was damaged. The "B" Loop of RHR was declared inoperable and Tech Specs Section 3.5.3.2 was implenented. Redundant systems ("A" Loop of RHR, Core Spray, HPIC, PCIC and ADS) were available and operable. There were no effects upon public health and safety due to this event. This is a non-repetitive event.

The motor breaker for the "B" Loop RHR Injection Valve tripped because of motor windings drew excessive current causing severe damage to the motor windings. The cause was attributed to unbalanced supply voltage and excessive torque requirements due to reactor pressure against the valve.

A LPCI inverter card was replaced to balance the voltage. The motor was replaced and the injection valve, 2E11-F015B. was then tested for operability and returned to service. Public health and safety was not affected by this event.

No inherent problems was found in the generic review.

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