ML20011A898

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LER 81-146/03L-0:on 810822,during Low Power Testing Prior to Initial Power Level Escalation,Auxiliary Feedwater Flow Gauges Disagreed W/Local Gauges within Tolerance Specified by Channel Check.Caused by Inadequate Design Change
ML20011A898
Person / Time
Site: McGuire Duke Energy icon.png
Issue date: 10/21/1981
From: Nardoci P
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20011A892 List:
References
LER-81-146-03L, LER-81-146-3L, NUDOCS 8111030333
Download: ML20011A898 (1)


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This violates T.S.3.3.3.6 which is reportable per T.S.6.9.1.13(b) .

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