ML20010F765

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LER 81-129/03L-0:on 810804,during Maint on Channel B Reactor Coolant Wide Range Instrumentation,Both RHR Trains Declared Inoperable When Inlet Isolation Valve Was Closed.Caused by Shut Signal Transmitted to Operator.Procedure Modified
ML20010F765
Person / Time
Site: McGuire Duke Energy icon.png
Issue date: 09/01/1981
From: Nardoci P
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20010F763 List:
References
LER-81-129-03L, LER-81-129-3L, NUDOCS 8109110303
Download: ML20010F765 (1)


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,,,3, irange pressure instrumentation., both trains of the Residual Heat Removal (ND) I

,,, , System were declared inoperable when an inlet isolation valve was inadvertently I

, .3 , 3 ; , closed. This is prohibited during Mode 5 operation by T.S. 3.4.1.4 which is 1 reportable pursuant to T.S. 6.9.1.13(b) and is similar to previous ROf/369/81-72.

,,,,,9 The loss of ND in this incident was momentary, and had no effect on the health

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,,,, , wide range pressure calibration procedure is being modified (and other proced ,

, , , . , tures checked) to ensure that required maintenance will have no adverse effects,

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  • I l,Z_,j@l N/A l r . . to NaC USE tNLY I:13i ,ba @$ssemirnca l N/Ah , tj,,,,,,,,,,l assusespaspaasn Phillip B. Nardoci ,,,c,,, (704) 373-7432 8109110303 810901 PDR ADOCK 05000369 PDR S _ __ ___ . , _ __