ML102110445

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IR 05000361-10-006; 05000362-10-006; on 10/01/2008 - 04/23/2010: San Onofre Nuclear Generating Station Biennial Baseline Inspection of the Identification and Resolution of Problems
ML102110445
Person / Time
Site: San Onofre  Southern California Edison icon.png
Issue date: 07/30/2010
From: Hay M
Division of Reactor Safety IV
To: Ridenoure R
Southern California Edison Co
References
EA-10-125 IR-10-006
Download: ML102110445 (73)


See also: IR 05000361/2010006

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION IV

612 EAST LAMAR BLVD, SUITE 400

ARLINGTON, TEXAS 76011-4125

July 30, 2010

EA-10-125

Mr. Ross T. Ridenoure

Senior Vice President and

Chief Nuclear Officer

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

SUBJECT: SAN ONOFRE NUCLEAR GENERATING STATION - NRC PROBLEM

IDENTIFICATION AND RESOLUTION INSPECTION

REPORT 05000361/2010006; 05000362/2010006 AND NOTICE OF VIOLATION

Dear Mr. Ridenoure:

On April 23, 2010, the U. S. Nuclear Regulatory Commission (NRC) completed the onsite

portion of a team inspection at your San Onofre Nuclear Generation Station. Additionally, the

inspectors performed in-office inspections through June 17, 2010. The enclosed report

documents the inspection findings discussed with you and members of your staff during an exit

briefing on June 17, 2010.

The inspection examined activities conducted under your license as they relate to identification

and resolution of problems, safety and compliance with the Commission's rules and regulations

and with the conditions of your operating license. The inspectors reviewed selected procedures

and records, observed activities, and interviewed personnel. The inspectors also interviewed a

representative sample of personnel regarding the condition of your safety conscious work

environment.

When compared with the findings from the previous inspection conducted in September 2008,

the findings from this inspection indicate that the corrective action program effectiveness has

declined. As previously discussed in the past 5 NRC assessment letters your staff's ability to

thoroughly evaluate problems such that the resolutions effectively address the causes and

extent of conditions is of concern. Your efforts to reverse the trend of substantive crosscutting

issues in both the human performance and problem identification and resolution areas have not

sho'lm to be effective.

The inspection identified a number of issues that your staff had previous opportunities to

identify. The Inspectors noted that even after issues were discussed with your staff thorough

evaluations were not consistently completed. We noted examples where your staff's

evaluations for deficient components failed to fully address component safety functions for all

applicable design basis accident scenarios.

Southern California Edison Company -2-

The inspectors reviewed the status of site corrective actions related to the areas of human

performance and problem identification and resolution described in your letters to the NRC

dated April 21, October 29, and October 30, 2009.

The inspectors noted examples where due dates were exceeded and different actions were

performed from those specified in the plan. As a result, the NRC identified a finding related to

your failures to meet the actions discussed in the above referenced letters. During the next

public meeting, that is currently being scheduled, you should address the status of your site

corrective actions and additional controls put in place to effectively monitor their execution. You

should also plan to address the causes for the inability to reverse the poor human performance

and problem identification and resolution trends.

This report documents ten NRC identified noncited violations, one NRC identified cited violation,

one self-revealing violation, and one finding, all of very low safety significance (Green).

Additionally, one licensee-identified violation is also discussed in this report. Because of the

very low safety significance of the violations and because they were entered into your corrective

action program, the NRC is treating these violations as noncited violations consistent with

Section VI.A.1 of the NRC Enforcement Policy. If you contest these noncited violations, you

should provide a response within 30 days of the date of this inspection report, with the basis for

your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington DC 20555-0001; with copies to the Regional Administrator, U.S. Nuclear

Regulatory Commission, Region IV, 612 E. Lamar Blvd., Suite 400, Arlington, Texas, 76011-

4125; the Director, Office of Enforcement, United States Nuclear Regulatory Commission,

Washington DC 20555-0001; and the NRC Resident Inspector at the San Onofre Nuclear

Generating Station.

The NRC-identified violation is cited in the enclosed Notice of Violation (Enclosure 1). The

violation involved the failure to revise and maintain in effect adequate procedures following plant

modifications. Although determined to be of very low safety significance (Green), this violation

is being cited in the Notice of Violation because not all of the criteria specified in Section VI.A.i

of the NRC Enforcement Policy for a non cited violation were satisfied. Specifically, San Onofre

Nuclear Generating Station failed to restore compliance within a reasonable time after

previously-identified noncited violations were identified in NRC Inspection Report 05000361;05000362/2009003-02 and 05000361;05000362/2009009-02. You are required to respond to

this letter and should follow the instructions specified in the enclosed Notice when preparing

your response. The NRC will use your response, in part, to determine whether further

enforcement action is necessary to ensure compliance with regulatory requirements.

If you disagree with the crosscutting aspect assigned to any finding in this report, you should

provide a response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region IV, and the NRC Resident Inspector at

San Onofre Nuclear Generating Station.

Southern California Edison Company -3-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRC's document system (ADAMS). ADAMS is accessible from the NRC Web-site at

www.nrc.gov/reading-rm/adams.html(the Public Electronic Reading Room). To the extent

possible, your response should not include any personal privacy, proprietary, or safeguards

information so that it can be made available to the Public without redaction.

Sincerely,

Michael C. Hay, Chief

Technical Support Branch

Division of Reactor Safety

Dockets: 50-361; 50-362

Licenses: NPF-10; NPF-15

Enclosures:

1. Notice of Violation

2. NRC Inspection Report 05000361/2010006; 05000362/2010006

w/Attachment: Supplemental Information

cc (w/Enclosures):

Chairman, Board of Supervisors

County of San Diego

1600 Pacific Highway, Room 335

San Diego, CA 92101

Gary L. Nolff

Assistant Director-Resources

City of Riverside

3900 Main Street

Riverside, CA 92522

Mark L. Parsons

Deputy City Attorney

City of Riverside

3900 Main Street

Riverside, CA 92522

Gary H. Yamamoto, P.E., Chief

Division of Drinking Water and

Environmental Management

1616 Capito! Avenue, MS 7400

P.O. Box 997377

Sacramento, CA 95899-7377

Southern California Edison Company -4-

Michael L. DeMarco

San Onofre Liaison

San Diego Gas & Electric Company

8315 Century Park Ct. CP21C

San Diego, CA 92123-1548

Director, Radiological Health Branch

State Department of Health Services

P.O. Box 997414 (MS 7610)

Sacramento, CA 95899-7414

The Mayor of the City of San Clemente

100 Avenida Presidio

San Clemente, CA 92672

James D. Boyd, Commissioner

California Energy Commission

1516 Ninth Street (MS 34)

Sacramento, CA 95814

Douglas K. Porter, Esquire

Southern California Edison Company

2244 Walnut Grove Avenue

Rosemead, CA 91770

Albert R. Hochevar

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

Steve Hsu

Department of Health Services

Radiologic Health Branch

MS 7610, P.O. Box 997414

Sacramento, CA 95899-7414

R. St. Onge

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

Chief, Technological Hazards Branch

FEMA Region IX

1111 Broadway, Suite 1200

Oakland, CA 94607-4052

Southern California Edison Company -5-

Institute of Nuclear Power Operations (lNPO)

Records Center

700 Galleria Parkway SE, Suite 10

Atlanta, GA 30339

NOTICE OF VIOLATION

Southern California Edison Company Docket No: 50-361; 50-362

San Onofre Nuclear Generating Station License No: NPF-10; NPF-15

EA-10-125

During an NRC inspection, conducted from April 5 to April 23, 2010, a violation of NRC

requirements was identified. In accordance with the NRC Enforcement Policy, the violation is

listed below:

Technical Specification 5.5.1.1.a requires, in part, that written procedures be

established, implemented, and maintained covering the applicable procedures

recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.

Regulatory Guide 1.33, "Quality Assurance Program Requirements (Operations),"

Appendix A, recommends procedures for the operation of certain plant systems.

Contrary to the above, prior to April 23, 2010, Southern California Edison Company

failed to maintain written procedures as recommended in Regulatory Guide 1.33,

Revision 2, Appendix A, February 1978. Specifically, the licensee failed to ensure that

following modifications made to the instrument air system the affected system

procedures where either suspended, put on administrative hold, or otherwise restricted

from use until the required changes were implemented. As a result, several procedures

with known technical deficiencies were inappropriately available for use following plant

modifications.

This violation is associated with a Green Significance Determination Process finding.

Pursuant to the provisions of 10 CFR 2.201, Southern California Edison Company is hereby

required to submit a written statement or explanation to the U.S. Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington, DC 20555-0001 with a copy to the

Regional Administrator, Region IV, and a copy to the NRC Resident Inspector San Onofre

Nuclear Generating Station, within 30 days of the date of the letter transmitting this Notice of

Violation (Notice). This reply should be clearly marked as a "Reply to Notice of

Violation EA-09-270," and should include: (1) the reason for the violation, or, if contested, the

basis for disputing the violation or severity level, (2) the corrective steps that have been taken

and the results achieved, (3) the corrective steps that will be taken to avoid further violations,

and (4) the date when full compliance will be achieved. Your response may reference or

include previous docketed correspondence, if the correspondence adequately addresses the

required response. If an adequate reply is not received within the time specified in this Notice,

an order or a Demand for Information may be issued as to why the license should not be

modified, suspended, or revoked, or why such other action as may be proper should not be

taken. Where good cause is shown, consideration will be given to extending the response time.

if you contest this enforcement action, you should also provide a copy of your response, with

the basis for your denial, to the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001.

Because your response will be made available electronically for public inspection in the NRC

Public Document Room or from the NRC's document system (ADAMS), accessible from the

- 1- Enclosure 1

NRC website at www.nrc.gov/reading-rm/pdr.html or www.nrc.gov/reading-rm/adams.html, to

the extent possible, it should not include any personal privacy, proprietary, or safeguards

information so that it can be made available to the public without redaction. If personal privacy

or proprietary information is necessary to provide an acceptable response, then please provide

a bracketed copy of your response that identifies the information that should be protected and a

redacted copy of your response that deletes such information. If you request withholding of

such material, you must specifically identify the portions of your response that you seek to have

withheld and provide in detail the basis for your claim of withholding (e.g., explain why the

disclosure of information will create an unwarranted invasion of personal privacy or provide the

information required by 10 CFR 2.390(b) to support a request for withholding confidential

commercial or financial information).

Dated this 30th day of July 2010.

2- Enclosure 1

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 50-361; 50-362

License: NPF-10; NPF-15

Report: 05000361/2010006; 05000362/2010006

Licensee: Southern California Edison Co.

Facility: San Onofre Nuclear Generating Station

Location: 5000 So. Pacific Coast Highway

San Clemente, California

Dates: April 5 through June 17, 2010

Team Leader: M. Vasquez, Senior Reactor Inspector, Technical Support Branch, DRS

Inspectors: C. Long, Senior Resident Inspector

R. Smith, Senior Resident Inspector

S. Walker, Senior Reactor Inspector

E. Ruesch, Resident Inspector

S. Matharu, Senior Electrical Engineer

G. Tutak, Project Engineer

Accompanied By: G. Wilson, Chief, Electrical Engineering Branch

S. Marquez, Nuclear Safety Professional Development Program

Approved By: Michael C. Hay, Chief

Technical Support Branch

Division of Reactor Safety

- 1- Enclosure 2

SUMMARY OF FINDiNGS

IR05000361 1201 0006; 05000362/2010006; October 1, 2008, through April 23, 2010:

San Onofre Nuclear Generating Station "Biennial Baseline Inspection of the Identification and

Resolution of Problems."

The report covers a 2-week period of onsite inspection by two senior resident inspectors, a

senior electrical engineer, a senior reactor inspector, a reactor inspector, and a project

engineer. Following the onsite inspection additional in-office reviews were performed through

June 17, 2010. The findings from this inspection include ten Green NRC identified noncited

violations, one Green self revealing violation; one Green cited violation, and one Green finding.

The significance of most findings is indicated by their color (Green, White, Yellow, Red) using

Inspection Manual Chapter 0609, "Significance Determination Process." Findings for which the

significance determination process does not apply may be Green or be assigned a severity level

after NRC management review. The NRC's program for overseeing the safe operation of

commercial nuclear power reactors is described in NUREG 1649, "Reactor Oversight Process,"

Revision 4, dated December 2006.

Identification and Resolution of Problems

The inspectors reviewed approximately 300 condition reports, work orders, engineering

evaluations, root and apparent cause evaluations, and other supporting documentation to

determine if problems were being properly identified, characterized, and entered into the

corrective action program for evaluation and resolution. The inspectors reviewed a sample of

system health reports, self-assessments, trending reports and metrics, and various other

documents related to the corrective action program.

When compared with the findings from the previous inspection conducted in September 2008,

the findings from this inspection indicate that the corrective action program effectiveness has

declined. As previously discussed in the past five NRC assessment letters, the licensee's ability

to thoroughly evaluate problems such that the resolutions effectively address the causes and

extent of conditions is of concern. The licensee's efforts to reverse the trend of substantive

crosscutting issues in both the human performance and problem identification and resolution

areas have not shown to be effective.

Additionally, the inspection identified a number of issues that the licensee's staff had previous

opportunities to identify. The inspectors noted that even after issues were discussed with the

licensees' staff, thorough evaluations were not consistently completed. We noted examples

were the evaluations for deficient components failed to fully address the component safety

functions for all applicable design basis accident scenarios.

The inspectors determined that the licensee adequately evaluated industry operating

experience for relevance to the facility, and entered applicable items in the corrective action

program. The inspectors noted that operating experience was considered in cause evaluations.

The inspectors noted that following the review of operating experience the licensee failed to

consistently incorporate the knowledge into procedural guidance and design calculations.

-2- Enclosure 2

In February 2010, the inspectors found that several work groups at San Onofre did not feel free

to raise safety concerns

without fear of retaliation. This was documented in NRC Inspection Report 050000361;

05000362/2009009 dated March 2, 2010, and in the NRC's Chilling Effect Letter dated March 2,

2010.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Initiating Events

II Green. The inspectors identified a noncited violation of Technical

Specification 5.5.1.1.a involving the failure of control room operators to follow

San Onofre Procedure S0123-0-A 1, "Conduct of Operations." These included

failures to: implement alarm response procedure place-keeping, announce

alarms to the control room supervisor, stop conversations when an alarm

annunciated and cleared, perform three-way communication during pre-job

briefing, review the summarize, anticipate, foresee, evaluate and review

questions during a pre-job brief, review the prerequisites of a procedure prior to

use, and remain cognitive of the re-activity change evolution by a control room

supervisor. This issue was entered into the licensee's corrective action program

as Nuclear Notification 200871332, and operations management immediately

began actions to institute a recovery plan to improve operator performance.

The finding was more than minor because it was associated with the Initiating

Events Cornerstone attribute of human performance, and it affected the

associated cornerstone objective to limit the likelihood of those events that upset

plant stability and that challenge critical safety functions during shutdown, as well

as during power operations. Using the Inspection Manual Chapter 0609,

"Significance Determination Process," Phase 1 Worksheet, the inspectors

concluded that the transient initiator did not contribute to both the likelihood of a

reactor trip and to the likelihood that mitigation equipment or functions would not

be available. As a result, the issue was of very low safety significance (Green).

The finding has a crosscutting aspect in the area of human performance

associated with the work practices because the licensee did not ensure

supervisory and management oversight of work activities.

H.4(c)(Section 40A2.5e)

II Green. The inspectors reviewed a self-revealing noncited violation of Technical

Specification 5.5.1.1.a involving the failure to maintain adequate instructions in

San Onofre Procedure S023-3-2.4, "RCS Purification and De-borating Ion

Exchanger Operation," Revision 21 to control borating of ion exchangers. The

failure to maintain an adequate procedure resulted in an unplanned power

reduction by control room operators. This issue was entered into the licensee's

corrective action program as Nuclear Notification 200721702. Immediate

corrective actions :ncluded revising the procedure and operator Cff9w training.

-3- Enclosure 2

The finding was more than minor because it was associated with the Initiating

Events Cornerstone attribute of human performance, and it affected the

associated cornerstone objective to limit the likelihood of those events that upset

plant stability and that challenge critical safety functions during shutdown, as well

as during power operations. Using the Inspection Manual Chapter 0609,

"Significance Determination Process," Phase 1 Worksheet, the inspectors

concluded that the transient initiator did not contribute to both the likelihood of a

reactor trip and to the likelihood that mitigation equipment or functions would not

be available. As a result, the issue was of very low safety significance (Green).

The finding has a crosscutting aspect in the area of human performance

associated with the work practices because licensee supervisory personnel did

not ensure activities associated with re-activity control were performed in a

controlled manner such that nuclear safety was assured.

H.4(c)(Section 40A2.5f)

  • Green. The inspectors identified a noncitied violation of Technical

Specification 5.5.1.1.a involving the failure to follow procedural guidance of

S0123-XX-11, "Switchyard Work Performance." Specifically, the inspectors

identified temporary equipment stored in the switchyard that was not tethered or

otherwise secured in accordance with the procedure. The licensee entered a

notification in its corrective action program as Nuclear Notification 200870138,

and removed or secured the items.

This finding is more than minor because it impacts the protection against the

external factors attribute of the Initiating Events Cornerstone objective to limit the

likelihood of those events that upset plant stability and challenge critical safety

functions during shutdown and power operations. Using the Inspection Manual

Chapter 0609 "Significance Determination Process," Phase 1 Worksheet, the

inspectors determined that the finding was of very low safety significance (Green)

because it did not contribute to both the likelihood of a reactor trip and the

likelihood that mitigation equipment or functions would not be available. This

finding also has a human performance crosscutting aspect associated with the

work control component in that personnel failed to appropriately plan work

activities involving job site conditions which may impact plant structures, systems

and components. H.3(a) (Section 40A2.5k)

Cornerstone: Mitigating Systems

Appendix B, Criterion V, "Instructions, Procedures, and Drawings,"

involving the failure to follow procedural requirements for performing

operability determinations. Specifically, the licensee's operability

evaluation for a degraded turbine-driven auxiliary feedwater pump steam

admission valve failed to address all the specified safety functions of the

affected component as described in the Final Safety Analysis Report and

design basis documents. For exampie, the operabiiity determination

incorrectly stated that manual closure of the valves was not a credited

-4- Enclosure 2

safety function and incorrectly assumed nonsafety-related instrument air

would always be available to close the valves. This finding was entered

into the licensee's corrective action program as Nuclear Notifications

200869281 and 200887620. The licensee's corrective actions included

re-performing the evaluation and emphasizing with licensee staff the

importance of ensuring ali design basis information is considered in

operability evaluations.

The finding was more than minor because it impacted the Mitigating

Systems Cornerstones and its objective to ensure the availability and

reliability of equipment that responds to initiating events. Using

Inspection Manual Chapter 0609 the issue screened to a Phase 3

analysis because it represented a loss of safety function for greater than

the allowed technical specification allowed outage time and it screened to

greater than Green using the Phase 2 pre-solved worksheet. The senior

reactor analyst determined that this finding was of very low safety

significance (Green) based on a bounding calculation which assumed

inoperability of the component for a year. The senior reactor analyst

determined that the combined significance of these scenarios was a

delta-core damage frequency of 1.3E-7/yr and a delta-large early release

frequency of 4.2E-8/yr. Therefore the violation was determined to be of

very low safety significance (Green). The analyst determined that the

cause of the finding has a crosscutting aspect in the area of human

performance associated with decision making. Specifically, the licensee

utilized unsupportable assumptions in its evaluation that were not

consistent with the Final Safety Analysis Report or the valve vendor

manual. H.1.b](Section 40A2.5a)

Appendix B, Criterion III, "Design Control" in that the licensee failed to translate

design basis information into procedures for the turbine-driven auxiliary

feedwater pump steam admission valves. Specifically, the licensee did not

translate into procedures the design requirements to manually close and gag the

valves within 30 minutes in response to high energy line breaks, a fire in the

auxiliary feedwater pump room, or a steam generator tube rupture event. This

issue was entered into the licensee's corrective action program as Nuclear

Notification 200887620. Immediate actions included posting a leveraging device

for operators to use should it be necessary, training operators, and scheduling

lubrication of the valves.

The finding is more than minor because it impacted the Mitigating Systems

Cornerstones and its objective to ensure the availability and reliability of

equipment that responds to initiating events. The analyst screened the issue to

more than one cornerstone due to its effect on early release (steam generator

tube rupture), fire protection, and mitigating systems (high energy line break).

The analyst performed a Phase 3 analysis that considered the effects of a high

energy line break in the pump room, a steam generator tube rupture, and fires in

-5- Enclosure 2

the pump room and auxiliary feedwater pipe tunnel. The analyst determined that

the combined significance of these scenarios was a delta- core damage

frequency of 5.E-9/yr and a delta- large early release frequency of 1.6E-9/yr.

Therefore, the violation was determined to be of very low safety significance

(Green). The inspectors determined that cause of the finding has a crosscutting

aspect in the area of problem identification and resolution associated with the

corrective action program. Specifically, the licensee had previous opportunities

to identify this problem when the valve was removed from the in-service testing

program and when they evaluated relevant external operating experience.

[P.i (a)j(Section 40A2.5b)

Green. The inspectors identified a noncited violation of Technical Specification 3.7.6, which requires, in part, that Condensate Storage Tank T-120

be operable. Specifically, the tank isolation valve 2HV5715 had been inoperable

for a period greater than the allowed outage time of seven days while Unit 2 was

in Modes 1, 2, and 3. The valve isolates nonseismic piping from the tank and is

required to be manually closed within 90 minutes following a seismic event. The

licensee had not performed preventive maintenance on the valve resulting in the

valve failing to close during an in-service test on January 26, 2010. This finding

was entered into the licensee's corrective action program as Nuclear

Notification 200765235. The licensee's corrective actions included repairing the

isolation valve.

This finding is more than minor because it impacted the Mitigating Systems

Cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

Using Inspection Manual Chapter 0609, Phase 1, "Initial Screening and

Characterization of Findings," a Phase 2 analysis was performed because the

condensate storage, Tank T-120, was inoperable greater than that allowed in

technical specifications. Phase 2 analysis resulted in a potential greater than

Green issue therefore, a Phase 3 was performed.

The analyst performed a Phase 3 using San Onofre seismic information and

fragility data associated with the piping that could not be isolated because of the

failed condition of valve 2HV5715. The frequency of a seismic event that would

cause a pipe break and drain tank T -120 was estimated to be 2.7E-5/yr. Given a

seismic event that causes a loss of offsite power (nearly 100 percent of seismic

events that rupture the piping would also cause a loss of offsite power), operators

are compelled by procedure to cool down and initiate shutdown cooling. The

amount of water that is protected with valve 2HV5715 failed to open, which

includes inventory from tank T-121 and water below the break line in tank T-120,

given that operators close the working manual isolation valve within 30 minutes,

is more than what is needed to get to shutdown cooling in natural circulation with

only 1 of 2 steam generator atmospheric dump valves in operation, even if there

is a 4-hour hold time at hot standby. The analyst estimated that the failure

probability of operators to coo! down and initiate shutdown coo!!ng is 1.0E-2.

Therefore, assuming a zero base case, the estimated delta- core damage

-6- Enclosure 2

frequency of the finding is 2.7E-5/yr. (1.0E-2) =2.7E-7/yr.

The inspectors also determined that the cause of the finding has a crosscutting

aspect in the area of human performance associated with resources in that the

licensee did not ensure that equipment was available and adequate to assure

nuclear safety by minimization of long-standing equipment issues in that the

valve was not being maintained through a preventive maintenance program.

H.2(a)(Section 40A2.5c)

  • Green. The inspectors identified a cited violation of Technical

Specification 5.5.1.1.a, involving the failure to maintain adequate written

procedures. Specifically, as of April 23, 2010, the licensee's controls over

its backlog of procedure change requests associated with plant

modifications were inadequate to prevent licensee personnel from using

outdated procedures with known technical errors in the plant. The

performance deficiency of failing to control the backlog of procedure

changes, such that procedures with known technical errors were in use in

the plant were previously identified by the NRC on two occasions and

were documented as non cited violations 05000361;05000362/2009003-09 and 2009009-02. Because the licensee failed to

restore compliance within a reasonable time after the previous non cited

violations were identified, this violation is being cited in a Notice of

Violation in accordance with Section Vl.a.1 of the NRC's Enforcement

Policy. This finding was entered into the licensee's corrective action

program as Nuclear Notification 200888919. The licensee's corrective

action included immediate actions to administratively suspend these

procedures until they could be revised and to evaluate changes needed

to its program to prevent recurrence.

The failure to maintain procedures covered by Regulatory Guide 1.33 is a

performance deficiency. The finding is of more than minor significance

because, if left uncorrected, the failure to maintain and control procedures

would have the potential to lead to a more significant safety concern.

Using Inspection Manual Chapter 0609, Phase 1,"Initial Screening and

Characterization of Findings," the finding was determined to have a very

low safety significance because the finding did not result in a loss of

system safety function, an actual loss of safety function of a single train

for greater than its technical specification allowed outage time, or screen

as potentially risk significant due to a seismic, flooding, or severe weather

initiating event. The finding has a crosscutting aspect in the area of

problem identification and resolution associated with the corrective action

program component, because problems were not thoroughly evaluated,

such that the resolutions addressed the causes and extents of condition.

This includes properly classifying and prioritizing conditions adverse to

quality. [P.i (c)](Section 40A2.5h)

-7- Enclosure 2

Green. Two examples of a noncited violation of 10 CFR 50.65(a)(1) were

identified involving the failure to monitor the unavailability time associated

with equipment failures which were maintenance induced. The first

example involved maintenance inadvertently bending the fuse holder

contacts such that there was a loose connection on the power supply on

the turbine-driven auxiliary feedwater pump resulting in its failure. The

second example involved the failure to perform maintenance associated

with a condensate storage tank isolation valve resulting in its failure

during in-service testing. In both cases, if the licensee had assessed the

unavailability time due to the maintenance induced failures, the systems

would have exceeded the 10 CFR 50.65(a)(2) monitoring criteria,

necessitating the systems to be placed in 10 CFR 50.65(a)(1) goal

setting. The licensee's corrective actions included evaluating its

procedures to prevent recurrence, and re-evaluating these systems to

determine the impact of accounting for unavailable time.

This finding is more than minor because it affects the equipment

performance attribute of the Mitigating Systems Cornerstone per

Inspection Manual Chapter 612, Appendix 8. Using Inspection

Manual Chapter 0609, Phase 1, "Initial Screening and Characterization of

Findings," the inspectors determined the finding to be of very low safety

significance (Green) because they did not represent the loss of a system

safety function and did not screen as potentially risk significant due to a

seismic, flooding, or severe weather initiating event The cause of the

finding was determined to have a crosscutting aspect in the area of

human performance. Specifically, personnel failed to use a formal

decision making process to determine how to count unavailable hours for

the maintenance rule. [H.i (a)](Section 40A2.5i)

Green. The inspectors identified a noncited violation of 10 CFR Part 50,

Appendix 8, Criterion XVI, "Corrective Action," in that, from October 2008

to April 2010, the licensee failed to promptly identify and correct

potentially degraded motor-driven relays in safety-related systems and

components. Specifically, after identifying a degraded relay affecting an

emergency diesel generator, the licensee replaced all similar relays in the

other diesel generators but failed to evaluate the use of these potentially

degraded relays in other safety-related systems. The licensee entered

this issue into the corrective action program as Nuclear

Notification 200146292, and developed a plan to replace the 62 degraded

relays that were installed in other safety-related equipment.

This finding was more than minor because it impacted the equipment

performance attribute of the Mitigating Systems Cornerstone objective to

ensure the availability, reliability, and capability of systems that respond

to initiating events to prevent undesirable consequences. Using

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Characterization of Findings," the inspectors determined the finding to be

-8- Enclosure 2

of very low safety significance (Green) because it did not represent the

loss of a system safety function and did not screen as potentially risk

significant due to a seismic, flooding, or severe weather initiating event.

This finding has a crosscutting aspect in the area of human performance

associated with the decision-making component, in that the licensee did

not use conservative assumptions in making decisions about the extent of

condition [H.1 (b)J(Section 40A2.Sj)

Green. The inspectors identified a noncited violation of 10 CFR Part SO,

Appendix B, Criterion III, "Design Control," involving the failure to translate

nonconservative errors in calculations and procedures identified during review of

external operating experiences. The first example involved the sizing calculation

for the condensate storage tank failing to account for effects of auxiliary

feedwater pump heat during recirculation. The second example involved the

failure to update procedural guidance concerning the adverse effects of placing

the low pressure safety injection system into operation following use of the

residual heat removal system in the shutdown cooling mode of operation above

200°F. This issue was entered into the licensee's corrective action program as

Nuclear Notification 20088626S. The licensee initiated actions to correct its

procedure and calculation for each instance.

The finding is of more than minor significance because it adversely affects the

design control attribute of the mitigating systems cornerstone objective. Using

Inspection Manual Chapter 0609.04, Phase 1, "Initial Screening and

Characterization of Findings," the finding was determined to have a very low

safety significance (Green) because the finding did not result in a loss of system

safety function, an actual loss of safety function of a single train for greater than

its technical specification allowed outage time, or screen as potentially risk

significant due to a seismic, flooding, or severe weather initiating event. The

finding has a crosscutting aspect in the area of problem identification and

resolution associated with the operating experience component because the

licensee failed to implement and institutionalize operating experience information,

including vendor recommendations, through changes to plant processes,

procedures, equipment, and training programs. P.2(b)(Section 40A2.SI)

Cornerstone: Public Radiation Safety

  • Green. The inspectors identified a noncited violation of Technical

Specification S.S.1.1.a, "Scope," involving the failure to establish

procedures for component cooling water system alignments such that

leakage of radionuclides to the environment would be monitored during all

operational alignments of component cooling water. Specifically,

radiation monitors could be aligned to only one train of component cooling

water at a time and the licensee's procedures had no provision for

monitoring the second train when both trains were in-service. This finding

was entered into the licensee's corrective action program as Nuc!ear

- 9- Enclosure 2

It Notification 200871387, and actions were implemented to require periodic

grab sampling of the train which was not being monitored.

The inspectors determined that this finding was more than minor because

this issue impacted the Public Radiation Protection Cornerstone and its

objective to ensure adequate protection of public health and safety from

exposure to radioactive materials released into the public domain as a

result of routine civilian nuclear reactor operation. Specifically, the

radiation monitors for component cooling water were not sufficient to

ensure adequate release measurements. The inspectors evaluated the

significance of this finding using Phase 1 of Inspection Manual Chapter 0609.04 and determined that the finding screened to Inspection

Manual Chapter 0609, Appendix D, "Public Radiation Safety Significance

Determination Process." The inspectors evaluated the significance of this

finding using Inspection Manual Chapter 0609, Appendix D, and

determined that the finding was of very low safety significance (Green)

because dose did not exceed Appendix I criteria. This finding was

determined to have a crosscutting aspect in the area of problem

identification and resolution associated with the corrective action program

in that the plant operators did not have a low threshold for identifying

deficiencies in procedures. [P.i (c)](Section 40A2.Sg)

Cornerstone: Miscellaneous

It Severity Level IV. The inspectors identified a Severity Level IV noncited

violation of 10 CFR SO.73, "Licensee Event Report System," in which the

licensee failed to submit a licensee event report within 60 days following

discovery of an event meeting the reportability criteria. On

January 26, 2010, the valve which isolates nonseismic piping from

condensate storage tank T -120 failed its in-service test when the hand

wheel stem snapped after a leveraging device was used in an attempt to

close the valve. This isolation valve, 2HVS71S, must be closed within 90

minutes of an operating basis earthquake in order to prevent the loss of

condensate storage tank T-120 water inventory from a line break in the

nonseismic portion of the condensate system. The failure of this valve

resulted in a condition prohibited by Technical Specification 3.7.6 and

therefore was reportable. This finding was entered into the licensee's

corrective action program as Nuclear Notification 200888616, and the

licensee was taking actions to send a licensee event report to the NRC

for this event.

The inspectors determined that traditional enforcement was applicable to

this issue because the NRC's regulatory ability was affected. Specifically,

the NRC reiies on the iicensee to identify and report conditions or events

meeting the criteria specified in regulations in order to perform its

regulatory function. The inspectors determined that this finding was not

suitable for evaluation using the significance determination process, and

- 10 - Enclosure 2

as such, was evaluated in accordance with the NRC Enforcement Policy.

The finding was reviewed by NRC management, and because the

violation was determined to be of very low safety significance, was not

repetitive or willful, and was entered into the corrective action program,

this violation is being treated as a Severity Level IV noncited violation

consistent with the NRC Enforcement Policy. This finding was

determined to have a crosscutting aspect in the area of problem

identification and resolution associated with the corrective action program

in that the licensee failed to appropriately evaluate corrective

maintenance as a basis for past operability. [P.1 (c)](Section 40A2.5d)

  • Green. The inspectors identified a Green finding associated with the

licensee's failure to meet the actions described to the NRC in letters

dated April 21,2009, and October 29 and 30, 2009, addressing corrective

actions to improve site performance in the areas of human performance

and problem identification and resolution. Specifically, 16 actions were

not implemented on time and a number of actions were modified from

what was previously described, all prior to informing the NRC. These

findings were documented in Nuclear Notification 200848923.

The inspectors determined that the licensee's failure to perform actions

as documented in its plan to the NRC was more than minor because if left

uncorrected could result in a more significant safety concern. Using

Inspection Manual Chapter 0609, Appendix M, this finding was reviewed

by NRC management and was determined to be of very low safety

significance (Green). This finding has a crosscutting aspect in the areas

of human performance. (Section 40A2.5m)

B. Licensee-Identified Violations

A violation of very low safety significance, which was identified by the licensee, has been

reviewed by the inspectors. Corrective actions taken or planned by the licensee have

been entered into the licensee's corrective action program. This violation and corrective

action tracking numbers (condition report numbers) are listed in Section 40A7.

- 11 - Enclosure 2

REPORT DETAilS

4. OTHER ACTIVITIES

40A2 Problem Identification and Resolution (71152)

The inspectors based the following conclusions on the sample of corrective action

documents that were initiated in the assessment period, which ranged from October 1,

2008, to the end of the on-site portion of this inspection on April 23, 2010 .

.1 Assessment of the Corrective Action Program Effectiveness

a. Inspection Scope

Approach and Scope: The inspectors visited San Onofre Nuclear Generating

Station from December 14 through 17, 2009, to review the sites corrective action

and maintenance backlogs. The backlog review included corrective actions,

maintenance actions and administrative actions involving pending procedure

changes.

The results of these reviews were used to select issues involving risk important

systems and operator actions that would be reviewed during future inspections.

The following areas were identified for future inspection:

.. Agastat relay failures

.. Medium voltage breakers conditions (safety related and nonsafety

related)

  • Switch yard transformers conditions

.. Backlog of pending procedure changes

.. Component power supplies problems

.. Aged electrolytic capacitors

  • High relay and breaker auxiliary contact resistance

e Electrical grounds

.. Emergency core cooling system voids

- 12 - Enclosure 2

It Reactivity control (chemical and volume control system)

.. Mitigating systems performance indicator trending

.. Component cooling water system voids

  • Component cooling water pump in runout conditions
  • Drifting undervoltage relays setpoint
  • DC Bus 301 low voltage
  • High pressure safety injection swing pump logic problems
Charging pump oil leaks
  • Pending plant modifications

.. Control room annunciator problems

.. Operator workarounds!operator burdens

The inspectors reviewed approximately 300 condition reports, including

associated root cause, apparent cause, and direct cause evaluations, that were

initiated between October 1, 2008, and April 5, 2010, to determine if problems

were being properly identified, characterized, and entered into the corrective

action program for evaluation and resolution. The inspectors also reviewed

system health reports, operability determinations, self assessments, trending

reports, metrics, and various other documents related to the corrective action

program. The inspectors reviewed work requests and attended the licensee's

corrective action review board and closure review board meetings to assess the

reporting threshold and prioritization processes. The inspectors' review included

verifying that the licensee considered the full extent of cause and extent of

condition for problems, as well as how the licensee assessed generic

implications and previous occurrences. The inspectors assessed the timeliness

and effectiveness of corrective actions, completed or planned, and looked for

additional examples of similar problems.

addressed past NRC-identified violations to ensure that the corrective actions

- 13- Enclosure 2

addressed the issues as described in the inspection reports. The inspectors

reviewed a sampie of corrective actions closed to other corrective action

documents to verify that corrective actions were appropriate and timely.

The inspectors considered risk insights to focus the sample selection and plant

tours on risk significant systems and components. Based on this review, the

samples reviewed by the inspectors focused on, but were not limited to, these

systems. The inspectors also expanded its review to include five years of

evaluations involving the salt water cooling system and various electrical

components to determine whether problems were being effectively addressed.

The inspectors conducted a walkdown of these systems to assess whether

problems were identified and entered into the corrective action program.

b. Assessments

i. Assessment - Effectiveness of Problem Identification

In general, the inspectors found that the licensee has been identifying

problems and entering them into their corrective action program at

appropriately low thresholds. For example, San Onofre Nuclear

Generating Station personnel had identified and initiated over 20,000

nuclear notifications into the corrective action process in 2009. The

inspectors identified many examples of failures to document problems

into the corrective action program resulting in missed opportunities for the

licensee to identify problems and adverse trends. In addition, there were

several issues that took significant NRC interaction with site staff in order

for them to recognize the problem. Examples of ineffective identification

of issues include the following:

  • The licensee failed to identify design basis information regarding

the steam admission valves to the turbine auxiliary feedwater

pump. On April 5, 2010, inspectors identified a concern that the

valves might not be able to be manually closed due to the

apparent lack of lubrication and rust on the Unit 3 valve stems

(3HV8200 and 3HV8201). These valves are normally held open

under spring pressure and are normally closed with nonsafety-

related instrument air. In cases where instrument air is not

available, the valve may be closed manually by rotating a hand

wheel approximately 24-25 rotations. The inspectors reviewed

design basis documents and the Final Safety Analysis Report and

found that the valves must be manually closed within 30 minutes

for certain accident sequences where instrument air is not

available. Based on the inspectors' concern that manually closing

the valve would be challenged with the lack of lubrication, San

Onofre Nuclear Generating Station conducted an operability

determination on April 10, 2010. Hovvever, the inspectors round

that the operability evaluation was inadequate and did not

- 14 - Enclosure 2

consider design basis information. After significant NRC

interaction, the licensee consulted with the vendor and found that

the valves could not be manually closed even under ideal

lubrication conditions because the force required to manually turn

the hand wheel exceeded the licensee's guideline for the amount

of force an individual could be expected to exert. Prior to the

inspectors' questioning, the licensee had failed to identify the force

needed to manually close the valve as well as other design basis

information. (Section 40A2.5b)

  • San Onofre Nuclear Generating Station failed to identify that the

failure of isolation valve 2HV5715 was reportable to the NRC.

This valve isolates nonseismic piping from the seismic piping on

condensate storage tank T-120. This valve must be closed within

90 minutes of an operating basis earthquake to prevent the tank

from draining its water through a postulated break in the

nonseismic piping. On January 26, 2010, an operator attempted

to perform the 2-year in-service test to manually stroke the valve

by rotating its hand wheel. When the hand wheel would not turn,

the operator followed procedure and contacted the control room to

obtain permission to use a leveraging device to turn the hand

wheel. When the operator used the leveraging device, the hand

wheel sheared off. San Onofre Nuclear Generator Station

reportability determination concluded the event was not reportable

because a mechanic could be called to disassemble the valve

actuator and manually close the valve with a wrench. During the

weeks of April 5 and April 19, the inspectors informed San Onofre

Nuclear Generator Station staff that this use of corrective

maintenance was inappropriate to consider for reportability

determination. The licensee maintained this position through a

"white paper" developed on May 7,2010. Subsequently, the

inspectors contacted the licensee and referred the licensee to the

specific guidance in NUREG 1022, whereby the licensee changed

its position. (Section 40A2.5d)

  • The licensee failed to identify that a nuclear notification had not

been written, as required by procedure, to document that a

leveraging device had been used when an operator sheared the

hand wheel off of the isolation valve (2HV5715) which isolates

nonseismic piping from the seismic piping on condensate storage

tank T-120. (Section 40A2.5c)

  • The inspectors questioned the ability of plant equipment operators

to identify plant problems during plant tours as a result of

knowledge deficiencies identified by the inspectors. On

AprH 7, 2010, inspectois obseived an experienced piant

equipment operator performing his daily rounds for several hours.

- 15 - Enclosure 2

The inspectors found that the nonlicensed operator did not

demonstrate fundamental knowledge regarding such items as

separation distances between scaffolding and safety-related

equipment, expected panel configurations, and requirements for

standard items like chocking carts. As a result, the inspectors

determined that given these knowledge weaknesses exhibited by

an experienced equipment operator they were limited in their

ability to identify plant problems.

  • The inspectors identified that some plant personnel appeared to

accept degraded or unacceptable conditions rather than

identifying the condition through the corrective action process and

getting them corrected. Examples included: (1) the common use

of leveraging devices which can mask degraded conditions;

(2) there were a number of control room alarms that had not been

cleared in preparation for the Unit 2 startup from the steam

generator replacement outage; (3) the inspectors identified that

one control room alarm had been locked in for four days because

data on a computer card needed to be downloaded; (4) after

inspectors questioned control room operators about the vibration

and loose parts monitor alarm, control room staff realized that they

were in day 5 of a 30-day action statement required by licensee

controlled specifications; and (5) the inspectors identified that

unsecured equipment in the switchyard that had been there for

months in violation of licensee procedures even though operators

had been performing routine rounds and others had been going in

and out of the area.

The inspectors noted that operators were not sensitive to a

condition involving the failure to have adequate procedures to

ensure that for all operational alignments of the component

cooling water system radiation monitoring would be in effect to

detect system leakage. (Section 40A2.5g)

.ii Assessment - Effectiveness of Prioritization and Evaluation of Issues

The inspectors found many instances where the licensee had correctly

prioritized and evaluated issues. In fact, there was objective evidence

that the quality of cause evaluations had improved during this inspection

period. However, the inspectors also found that San Onofre Nuclear

Generating Station continued to have significant challenges performing

these actions consistently. While most initial operability determinations

were appropriate, the inspectors identified several examples where poor

evaluations were performed. The following are examples of ineffective or

inadequate evaluation of issues:

- 16 - Enclosure 2

San Onofre Nuclear Generating Station staff performed an

inadequate evaluation of the reportability of the failure of the

isolation valve for condensate storage tank T-120.

(Section 40A2.5d)

San Onofre Nuclear Generating Station staff performed an

inadequate operability determination of the steam admission

valves to the turbine-driven auxiliary feedwater pumps after the

inspectors raised concerns about lack of stem lubrication.

(Section 40A2.5a)

  • San Onofre Nuclear Generating Station staff performed an

inadequate extent of condition evaluation involving potentially

degraded Potter & Brumfield motor driven rotary relays.

(Section 40A2.5j)

electrical connection in high pressure safety injection motor

cubicle 2A0608. Specifically, the method used to evaluate the

circuit continuity did not properly take into account the circuit

operation. The licensee initiated Nuclear Notification 200871532

on April 9, 2010, to evaluate the inspector's concern.

  • The inspectors reviewed a root cause, three apparent causes, and

one common cause evaluation dealing with operators failing to

properly make correct operability determinations. In one example,

operators failed to declare an atmospheric dump valve inoperable

based on testing results and failed to write a nuclear notification

when the degraded conditions changed. Additionally, the

inspectors identified that the licensee had also failed to implement

all its corrective actions associated with this example.

iii. Assessment - Effectiveness of Corrective Action Program

The inspectors concluded that actions to correct conditions adverse to

quality were generally adequate; however, there were notable examples

where the licensee had not implemented effective corrective actions.

Some examples included:

  • Licensee actions to correct substantive crosscutting issues have

not been effective. Despite actions to reverse the trend, San

Onofre Nuclear Generating Station has experienced five

consecutive assessment cycles with an increasing number of

sUbstantive crosscutting issues.

.. San Onofie Nuclear Generating Station actions have not been

effective in responding to two previously issued NCVs dealing with

- 17 - Enclosure 2

prioritizing the large backlog of procedure change requests.

During this inspection, the inspectors found that procedure

changes were not implemented following modifications to the

instrument air system. The inspectors concluded that San Onofre

Nuclear Generator Station corrective action to two previously

issued noncited violations for the same issue were not fully

effective. This violation is being cited as a Notice of Violation.

(Section 40A2.Sh)

  • The licensee's actions to improve the conduct of operations in the

control room have not been effective based on control room

observations, which identified ineffective use of place keeping,

use of 3-way communications, announcing alarms to the control

room supervisor, and review of prerequisites prior to procedures

being implemented. (Section 40A2.Se)

.2 Assessment of the Use of Operating Experience

a. Inspection Scope

The inspectors examined the licensee's program for reviewing industry operating

experience, including reviewing the governing procedure and self-assessments.

A sample of operating experience notification documents that had been issued

during the assessment period were reviewed to assess whether the licensee had

appropriately evaluated the notification for relevance to the facility. The

inspectors also examined whether the licensee had entered those items into their

corrective action program and assigned actions to address the issues. The

inspectors reviewed a sample of root cause evaluations and significant condition

reports to verify if the licensee had appropriately included industry operating

experience.

b. Assessment

Overall, the inspectors determined that the licensee had appropriately evaluated

industry operating experience for relevance to the facility, and had entered

applicable items in the corrective action program. The inspectors noted that

operating experience was considered in cause evaluations. The licensee failed

to incorporate two of the four operating experience evaluation results into plant

operating procedures and design documents. This is documented as a violation

of 10 CFR Part SO, Appendix B, Criterion III. (Section 40A2.SI)

.3 Assessment of Self-Assessments and Audits

a. Inspection Scope

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assess whether the licensee was regularly identifying performance trends and

- 18 - Enclosure 2

effectively addressing them. The inspectors also reviewed audit reports to

assess the effectiveness of assessments in specific areas. The specific self-

assessment documents and audits reviewed are listed in the attachment.

b. Assessment

The inspectors concluded that the licensee had an effective self-assessment

process. Licensee management was involved in developing the topics and

objectives of self-assessments. Attention was given to assigning inspectors

members with the proper skills and experience to do an effective

self-assessment and to include people from outside organizations. Audits were

self-critical and identified deficiencies in various programs such as the corrective

action program and the equipment reliability program .

.4 Assessment of Safety-Conscious Work Environment

a. Inspection Scope

From February 1-10, 2010, a inspectors conducted 40 focus group sessions

consisting of approximately 8-10 individuals each. The focus groups were

conducted to assess the safety-conscious work environment at the San Onofre

Nuclear Generating Station. The results of the focus groups were documented in

NRC Inspection Report 05000361 ;05000362/2009009 dated March 2, 2010, and

in the NRC's Chilling Effect Letter issued to San Onofre dated March 2, 2010.

b. Assessment

As documented in the NRC's March 2, 2010, Chilling Effect Letter, the NRC

concluded that some employees in multiple workgroups at San Onofre Nuclear

Generating Station have the perception that they are not free to raise safety

concerns using all available avenues, and that management has not been

effective in encouraging employees to use all available avenues without fear of

retaliation. This conclusion resulted from numerous observations, including:

(1) employees expressing difficulty or inability to use the corrective action

program; (2) a lack of knowledge or mistrust of the Nuclear Safety Concerns

Program (NSCP); (3) a substantiated case of a supervisor creating a chilled work

environment in his/her work group; and (4) a perceived fear of retaliation for

raising safety concerns. The licensee replied by letter dated March 31, 2010.

Further actions by the NRC are discussed in the March 2 letter.

.5 Specific Issues Identified During This Inspection

a. Inadequate Operability Determination for Turbine-Driven Auxiliarv Feedwater

Pump Steam Admission Valves

Intrnc!uctinn. A Green noncited violation of 10 CFR Part 50, Appendix 8,

Criterion V, "Instructions, Procedures, and Drawings," was identified involving the

failure to perform an adequate operability determination as required by

- 19 - Enclosure 2

procedure. Specifically, the licensee's operability evaluation for a degraded

turbine driven auxiliary feedwater pump steam admission valve failed to address

all the specified safety functions of the affected component as described in the

final safety analysis report and design basis documents.

Description. On April 7, 2010, inspectors noted what appeared to be

unlubricated valve stems on the Unit 3 steam admission valves to the turbine-

driven auxiliary feedwater pump, which are designated as 3HV8200 and

3HV8201. These valves are normally held open by spring pressure and are

normaiiy ciosed with nonsafety-related instrument air. The design basis requires

that for certain accident sequences in which the nonsafety-related instrument air

system is unavailable, these valves must be manually closed within 30 minutes.

The valves are manually closed by turning their respective hand wheel about

25 rotations. The valves are provided with manual gagging (locking) devices to

force the valves closed without instrument air and to lock the valves closed, such

that they won't inadvertently re-open. The inspectors were concerned that

increased friction from an unlubricated valve stem would make turning the hand

wheel against the spring force more difficult during manual operation.

The inspectors identified the issue to the licensee and noted that design basis

documents required the valves be manually closed and "gagged" or locked in the

following accident scenarios: (1) a high energy line break in the auxiliary

feedwater pump room; (2) a steam generator tube rupture; and (3) a fire in the

auxiliary feedwater pump room. The inspectors also discussed the design bases

with the licensee. As a result of the inspectors' concern, the licensee initiated

Nuclear Notification 200869281, and on April 8, 2010, commenced an operability

determination. On April 10, 2010, San Onofre personnel completed the

operability determination and concluded that the unlubricated gagging devices

were operable. However, the inspectors found that the operability determination

was inadequate.

The operability determination concluded that the valves were used in the postfire

safe shutdown analysis which was addressed by the notification, but did not

address the impact on technical specification operability. The operability

determination stated that the valves could be manually closed and gagged but it

provided no technical basis for the statement. Inspectors reviewed San Onofre

Procedure S0123-XV-52, "Functionality Assessments and Operability

Determinations," Revision 15. Step 6.5.1 required that the immediate operability

determination identify the specified safety function of the affected system,

structure or component. Step 6.5.1.3.2 stated that the operability determination

must identify the performance parameter used to determine operability.

Inspectors found that the April 10, 2010, operability determination was

inadequate because it failed to identify the performance parameters used to

determine operability; specifically, the design basis for these valves.

Inadequacies included:

- 20 - Enclosure 2

i. The determination incorrectly stated, "Manual closure of 2HV8200 and

2HV8201 is not a credited safety function of these valves for emergency

operating events." This was contrary to Final Safety Analysis Report

Table 10.4-7, which described use of the valves during a high energy line

break without the use of instrument air. Final Safety Analysis Report

Section 15.6.3, described valve closure and release termination within

30 minutes of a steam generator tube rupture. Design Basis Document

SD-S023-780 also described the manual action to gag the valves closed.

ii. The determination incorrectly assumed that nonsafety-related instrument

air would always be available to stroke the valves closed from the control

room.

iii. The determination incorrectly assumed the valves are closed against zero

opposing force to prevent them from re-opening on an auxiliary feedwater

start signai.

iv. The determination cited a procedure that only stated to close the valve,

but the procedure did not state during which events the valves should be

closed. This instruction was apparently only used during maintenance of

the valves or terry turbine.

Based on interviews, operations and engineering were not specifically aware that

the valves needed to be manually gagged closed even though the inspectors

discussed the design basis with other licensee personnel. After additional

inspectors' questioning and re-review of the design basis and the gag operation

with San Onofre Nuclear Generating Station personnel, San Onofre Nuclear

Generating Station re-performed the operability determination under Nuclear

Notification 20088760 and completed it on April 21, 2010. Based on the second

operability determination, which included contacting the vendor, licensee

personnel informed the inspectors on April 22, 2010, that the valves were

declared inoperable and that the licensee was taking interim compensatory

corrective actions. Thus, the licensee's initial operability determination on April

10, 2010, had been inadequate even after the inspectors had discussed the

design basis with licensee personnel prior to the licensee's evaluation.

The licensee documented this violation in Nuclear Notification 20088760, and its

short term corrective actions included required training and the staging of a

leveraging device in the vicinity of the valves to assist operators in closing and/or

gagging the valves, as required.

Analysis. Inspectors found that the failure to perform an adequate operability

determination and to identify the degraded condition was a performance

deficiency. The deficiency was more than minor because it impacted the

Mitigating Systems Cornerstones and its objective to ensure the availability and

reliability of equipment that responds to initiating events. Using Inspection

Manual Chapter 0609, the issue screened to Phase 3 because it represented a

loss of safety function for approximately two weeks and it screened to greater

- 21 - Enclosure 2

than Green using the Phase 2 pre-solved worksheet. The inspectors determined

that the finding was Green based on the bounding analyses discussed in the

analysis section of 40A2.5b. Specifically, this vulnerability existed for

approximately two weeks (the time between the inadequate evaluation and the

correct evaluation), which is considerably less than the one year vulnerability

discussed in the analysis section of 40A2.5b. The inspectors determined that the

cause of the finding has a crosscutting aspect in the area of human performance

associated with decision making. Specifically, San Onofre Nuclear Generating

Station utilized unsupportable assumptions in its evaluation that were not

consistent with the Final Safety Analysis Report or the valve vendor manual.

[H.i.b]

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, requires, in part,

that activities affecting quality be prescribed by procedures and be accomplished

in accordance with those procedures. San Onofre Procedure S0123-XV-52,

"Functionality Assessments and Operability Determinations," Revision 15,

Step 6.5.1 requires, in part, that the immediate operability determination identify

the specified safety function of the affected system, structure or component. San

Onofre Procedure S0123-XV-52 Step 6.5.3.1 requires, in part, that the

operability determination must identify the performance parameter used to

determine operability. Contrary to the above, from April 10 to April 22, 2010, San

Onofre Nuclear Generating Station performed an inadequate operability

determination required by San Onofre Procedure S0123-XV-52. Specifically,

San Onofre Nuclear Generating Station failed to identify the design basis

parameters for the steam admission valves for the turbine-driven auxiliary

feedwater pumps as described in the Final Safety Analysis Report and design

basis documents. In accordance with the NRC's Enforcement Policy, because

the violation was of very low safety significance, and was entered into the

corrective action program as Nuclear Notification 20088760, this violation is

being treated as noncited violation, consistent with the NRC Enforcement

Policy VI.A: NCV 05000361/2010006-01, "Inadequate Operability Determination

for turbine-driven auxiliary feedwater pump steam admission valves."

b. Failure to Translate Design Basis Information for Closure of Turbine-Driven

Auxiliary Steam Admission Valves

Introduction. On April 7, 2010, inspectors identified a Green noncited violation of

10 CFR Part 50, Appendix B, Criterion III, "Design Control," for steam admission

valves to the turbine-driven auxiliary feedwater pumps that could not be closed

within 30 minutes per the design basis.

Description. As discussed in the previous section, on April 7, 2010, inspectors

found apparently unlubricated valve stems on the Unit 3 steam admission valves

to the turbine-driven auxiliary feedwater pump, which are designated as

3HV8200 and 3HV8201. The inspectors identified a Green noncited violation

related to the inadeauate ooerabilitv determination that lir:en!=:eA OAr!=:()nnAI

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performed on April 10, 2010.

- 22- Enclosure 2

On April 22, 2010, after performing a second operability determination, the

licensee representatives informed the inspectors that they had contacted the

vendor and found the valves were inoperable because a person would not be

able to manually close and gag the valves under ideal lubrication conditions. The

licensee's standard was that a person would be able to apply a force of up to

100 pounds. However, ideally lubricated valves would require 132 pounds of

force on the hand wheel, and the hand wheel would have to be turned

approximately 25 times in order to close and gag the valve. The increased

friction from lack of lubrication and disc-in-seat forces could exceed 200 pounds

of force on the hand wheel. As a result of this information, the licensee began

taking corrective actions by posting leveraging devices for operators to use in the

event manual closure of the valves was needed. On April 22, 2010, required

reading on valve operation was implemented to train all licensed and non licensed

operators on the valve operation.

For postfire safe shutdown procedures, damage to the 2(3)HY8200 and

2(3)HY8201 solenoid valves associated circuit cables routed to auxiliary relay

cabinet L071 could cause a loss of the ability to close the air-

operated 2(3)HV8200 and 2(3)HV8201 from the control room. San Onofre

Procedure S023-13-21 "Fire" provided instructions for operators to mitigate the

effects of fire damage to safe shutdown equipment in plant areas. The steam

admission valves are required to be closed within 30 minutes of a fire by the

postfire safe shutdown analysis. Based on the April 22, 2010, operability

determination, the licensee added steps to San Onofre Procedure S023-13-21 to

use a crescent wrench and leverage device. These tools were locally staged to

back off the hand wheel stem nut and then use the leverage device on the hand

wheel to force the gag to shut the valve against its opening spring. The

inspectors concluded that prior to April 22, 2010; manual actions could not have

been taken within the 30-minute period because of the lack of tools and the

operator's lack of familiarity with San Onofre Procedure S023-13-21 which

identified key manual actions needed.

The inspectors noted the following prior opportunities the licensee had to identify

this deficiency:

i. In 2004, Action Request 040700869 erroneously stated that the safety

function to close the 8200 valves was not required in the design basis

document.

ii. In 2005, Action Request 050700659 was written to request that design

engineering delete the manual closure of the valves from the ASME O&M

Code in-service testing based on an incorrect evaluation which stated that

the valves were not part of the accident analysis. The action request also

erroneously stated the valves would not impact other programs such as

fire protection.

iii. On November 19, 2009, the licensee failed to identify this issue during its

review of Operating Experience 30062, "Locally Operated Time Critical

- 23 - Enclosure 2

Valves May be Difficult to Operate Under Accident Conditions" which

dealt with the possibility that the expected differential pressure across

locally operated valves must be considered when evaluating the ability of

operators to change valve positions in accident conditions. The operating

experience stated that this evaluation should be similar to the review

required by Generic Letter 89-10 for valves locally operated under high

differential pressure.

On April 22, 2010, San Onofre Nuclear Generating Station's corrective

action was to post leveraging devices and to schedule lubrication of the

valves for August 2010. The NRC considered immediate lubrication to be

an important corrective action that the licensee had not adequately

addressed while the inspectors were onsite. In addition, because a dry

lubricant was used on the valve (in accordance with the manufacturer's

recommendations) and the valve was exposed to the weather, the

inspectors also questioned the 10 year frequency for lubrication. Based

on further questioning from the inspectors, on May 25, 2010, the licensee

wrote Nuclear Notification 200937258 to address the inspectors' concern

about the adequacy of lubrication of the valve stem as well as the

frequency of lubrication.

The inspectors concluded that prior to April 22, 2010; the 8200 series

valves had been inoperable because the licensee had not translated the

design basis into procedures. The licensee did not translate into its

procedures the design bases requirements to manually close the valves

within 30 minutes of the required accident scenarios and did not consider

the force needed to manually close and gag the valves. Inspectors also

found that the licensee was not meeting Licensee Controlled Specification

Surveillance Requirement 3.7.113.1.12 to manually stroke the valve every

24 months to ensure compliance with the fire protection program. In

addition, simulated operator actions during a walkthrough of San Onofre

Procedure S023-13-21, "Fire," could not be performed in the time

specified in engineering calculations, nor were all appropriate steps

specified. The licensee was also evaluating necessary actions for a

permanent corrective action to this issue.

Analysis. The inspectors found that the failure to translate design basis

information regarding the 2(3)HV8200 and 2(3)HV8201 valves into procedures

was a performance deficiency. The deficiency was more than minor because it

impacted the Mitigating Systems Cornerstones and its objective to ensure the

availability and reliability of equipment that responds to initiating events. The

inspectors screened the issue to more than one cornerstone due to its affect on

early release (steam generator tube rupture), fire protection, and mitigating

systems (high energy line break).

Appendix H, because the finding represents an actual open pathway in the

physical integrity of reactor containment during a steam generator tube rupture

- 24- Enclosure 2

accident scenario. In Inspection Manual Chapter 0609 Appendix H, Step 4.1, the

inspectors screened this as a Type B finding (affects large early release fraction

but not core damage frequency) needing a Phase 2 evaluation. Inspectors used

Table 4.1 and found that the finding involved a large release path from the

reactor coolant system to the environment. Using Table 6.2, inspectors screened

the Phase 2 to greater than Green because the condition existed for greater than

one year and the volume of steam released would be larger than the free volume

of containment.

The inspectors screened the issue to Phase 2 for at-power inspection findings

using Inspection Manual Chapter 0609 because the turbine-driven auxiliary

feedwater valves could not be closed within 30 minutes after a high energy line

break to prevent failure of the two remaining auxiliary feedwater pumps. This

represented the potential loss of a safety function.

Inspectors screened the issue to Phase 2 for Appendix F of Inspection Manual

Chapter 0609 because the valves could not be closed for a fire in the auxiliary

feedwater room.

The senior reactor analyst performed a Phase 3 analysis to determine the risk

significance of the degraded turbine-driven auxiliary feedwater steam admission

valve. The analysis considered the effects of a high energy line break in the

pump room, a steam generator tube rupture, and fires in the pump room and

auxiliary feedwater pipe tunnel. The inspectors determined that the combined

significance of these scenarios was a delta-core damage frequency of 1.3E-7/yr

and a delta-large early release frequency of 4.2E-B/yr. Therefore, the violation

was determined to be of very low significance.

The violation has a crosscutting aspect in the area of problem identification and

resolution associated with the corrective action program. Specifically, the

licensee had multiple opportunities to evaluate this problem but failed to do so.

[P.1 (a)]

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion III, "Design Control"

requires, in part, that the design basis for systems, structures, and components

be correctly translated into specifications, drawings, and procedures. Contrary to

the above, prior to April 22, 2010, the licensee failed to translate the following

design basis information into procedures: (1) the requirements to manually close

and gag within 30 minutes the steam admission valves for the turbine driven

auxiliary feedwater pump in response to high energy line breaks or steam

generator tube rupture; and (2) the failure to determine the forces required to

manually close the valves. Because the violation was of very low safety

significance (Green), and was entered into the corrective action program as

Nuclear Notification 200B70B61 this violation is being treated as a non cited

violation, consistent with the NRC Enforcement Policy section VI.A:

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turbine-driven auxiliary feedwater pump Steam Admission Valves."

- 25 - Enclosure 2

c. Lack of Preventive Maintenance Results in Valve Failure of Condensate Storage

Tank

Introduction. A Green noncited violation of Technical Specification 3.7.6 was

identified which requires, in part, that condensate storage tank T-120 be

operable. Specifically, the tank isolation valve 2HV5715 had been inoperable for

a period greater than the allowed outage time of seven days while Unit 2 was in

Modes 1,2, and 3. The valve isolates nonseismic piping from the tank and is

required to be manually closed within 90 minutes following a seismic event. The

licensee had not performed preventive maintenance on the valves resulting in the

valves failing to close during an in-service test on January 26, 2010.

Description. On January 26, 2010, the hand wheel on the Unit 2 condensate

storage tank manual valve 2HV5715 broke while licensee personnel attempted to

perform an in-service test. This valve isolates nonseismic from seismic piping

supporting condensate storage tank T -120. The design basis for the valve is to

be closed within 90 minutes of an operating basis earthquake in order to

preserve the water inventory in condensate storage tank T -120. The water

inventory in that tank is needed to provide a water source for the auxiliary

feedwater pumps to remove heat from the reactor. A line break in the

nonseismic portion of the condensate system could drain tank T-120 of its water

inventory, which is required to support plant cooldown from Mode 1 to Mode 5.

Final Safety Analysis Report 10.4.9.2.3.4, "Emergency Operation," states that

tank T-121 is the primary source of auxiliary feedwater condensate with tank

T-120 required for backup.

The licensee employee performing the in-service test attempted to cycle the

valve but was not able to rotate the hand wheel. So, in accordance with

procedures, the licensee contacted the control room and obtained permission to

use a leveraging device to turn the valve. When the licensee employee applied

the leveraging device to the hand wheel, it sheared the pin connecting the hand

wheel to the valve manual actuator stem. The valve was repaired the next day.

During the subsequent diagnostics, the actuator stem was found to be heavily

rusted and without lubrication. The licensee employee determined that the valve

had been inadvertently removed from the preventive maintenance program

several years prior.

At the time the valve failed, Unit 2 was in an outage and the valve was not

required to be operable. Nuclear Notification 200765235 stated that the valve

was inoperable and could not fulfill its safety function to preserve the water

inventory in condensate storage tank T-120. However, in determining past

operability, emails were attached to Nuclear Notification 200765235 that stated

that corrective maintenance could be performed to open the valve; specifically,

that a mechanic could have been called upon to disassemble the valve actuator

and manually close the valve. Thus, the licensee concluded the valve was

operable prior to January' 26, 2010, and that the failure vvas not reportable.

- 26- Enclosure 2

The inspectors challenged the licensee in its determination that the valve had

been operable prior to the hand wheel breaking and that the failure was not

reportable to the NRC. The inspectors' position was that it was inappropriate to

consider corrective maintenance in the reportability determinations. The licensee

originally maintained its position asserting that the valve was operable and that

the issue was not reportable, again basing its decision on corrective

maintenance. After the inspectors referred the licensee to appropriate NRC

guidance in NUREG-1022, the licensee determined that the broken valve had not

been operable prior to the event and that the event was reportable.

The inspectors also challenged the use of leveraging devices on isolation

valve 2HV5715 as well as other manually-operated valves. Several other

manual valve hand wheels in the area had markings indicative of extensive use

of leveraging devices. Inspectors were informed that nuclear notifications were

not being written each time leveraging devices were used on manual valves,

which was required in accordance with Procedure S0123-0-A6, "Routine

Equipment Operations," Revision 8. San Onofre Nuclear Generating Station is

re-examining its in-service testing periodicity and preventive maintenance

practices in Nuclear Notification 200952866. The inspectors also noted that a

nuclear notification had not been written, as required, when the leveraging device

was used on isolation valve 2HV5715 on January 26, 2010.

In order to determine whether the licensee could reasonably close the valve

within 90 minutes of an operating basis earthquake, inspectors performed a

walkdown of the actions licensee staff would take following a seismic event. The

inspectors interviewed licensee staff who had not been informed of the

inspectors question prior to the walk down. The inspectors proposed a scenario

to the shift manager that the plant experienced an operating basis earthquake

and assessed the time it would have taken before she/he would have contacted

the maintenance general foreman to fix isolation valve 2HV5715. The inspectors

then interviewed the maintenance general foreman in order to understand what

she/he would do for this situation. The inspectors also interviewed three

mechanics and gave them the scenario conditions. Reviewing the time line

starting 90 minutes after the earthquake, the inspectors determined the total time

to close the valve was approximately 105 minutes. Based on this data, the

inspectors raised the concern to the licensee that its staff would be unable to

meet its design basis for cloSing this valve following an operating basis

earthquake.

Subsequent to the inspection, the licensee ran this scenario in the simulator

(without announcing it to the crew in advance). The results were that it took the

crew an estimated 134 minutes to have a mechanic manually turn the valve.

Therefore, the licensee determined that its staff could not complete manually

closing the valve within the 90 minute time frame required by the design basis,

and began taking actions to review its licensing basis and its procedures, and

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- 27- Enclosure 2

The isolation valve was last stroked in March 2008, and the licensee could not

determine the exact date the valve became inoperable. Given the failure mode,

the inspectors concluded that the valve had been inoperable for greater than

seven days when the licensee was last in Mode 1,2 or 3, when the valve was

required to be operable.

The licensee documented this deficiency in Nuclear Notification 200765235, and

repaired the valve and placed it into the preventive maintenance program.

Analysis. The inspectors determined that the failure to perform preventive

maintenance, including lubricating the valve actuator's components necessary to

manually close valve 2HV5715, was a performance deficiency. This issue is

more than minor because it impacted the Mitigating Systems Cornerstone

objective to ensure the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences (Le., core

damage). Specifically, the broken valve impacted the protection against external

events attribute for seismic protection. The inspectors used Inspection Manual

Chapter 0609, "Initial Screening and Characterization of Findings," to analyze the

significance of this finding. The inspectors screened the finding to Phase 2

because the condensate storage tank T -120 was inoperable for a significant

period greater than that allowed in technical specifications (using the time over

two methodologies, the tank was inoperable for approximately a year). This

screened the finding out of Phase 2 to Phase 3 because the closest surrogate for

this deficiency was failure of one of the auxiliary feedwater pumps for one year

which screened to red. A Phase 3 analysis was performed by the senior reactor

analyst. Using San Onofre Nuclear Generating Station's seismic information and

fragility data associated with the piping that could not be isolated because of the

failed condition of valve 2HV5715, the frequency of a seismic event that would

cause a pipe break and drain tank T-120 was estimated to be 2.7E-5/yr. Given a

seismic event that causes a loss of offsite power (nearly 100 percent of seismic

events that rupture the piping would also cause a loss of offsite power), operators

are compelled by procedure to cool down and initiate shutdown cooling. The

amount of water that is protected with valve 2HV5715 failed open, which includes

inventory from tank T-121 and water below the break line in tank T-120, given

that operators close the working manual isolation valve within 30 minutes is more

than what is needed to get to shutdown cooling in natural circulation with only

one of two steam generator atmospheric dump valves in operation, even if there

is a 4-hour hold time at hot standby. The analyst estimated that the failure

probability of operators to cool down and initiate shutdown cooling is 1.0E-2.

Therefore, assuming a zero base case, the estimated delta-core damage

frequency of the finding is 2.7E-5/yr. (1.0E)=2.7E-7/yr.

The inspectors also determined that the cause of the finding has a crosscutting

aspect in the area of human performance associated with resources in that San

Onofre Nuclear Generating Station did not ensure that equipment was available

and adequate to assure nuclear safety by minimization of fong-standing

equipment issues in that the valve was not being maintained through a

preventive maintenance program. H.2(a)

- 28- Enclosure 2

Enforcement. Technical Specification 3.7.6 requires, in part, that tank T-120 to

be operable. Valve 2HV5715 is required for tank operability because it must be

closed after an earthquake to preserve tank inventory. Condition C provides for

a completion time of seven days. Contrary to the above, prior to

January 26, 2010, valve 2HV5715 could not be closed for greater than its

completion time of seven days. The valve was failed in the open position.

Because this violation was of very low safety significance and was entered into

the licensee's corrective action program under Nuclear Notifications 200765235.

This violation is being treated as a noncited violation, consistent with Section

VI.A of the NRC Enforcement Policy: NCV 05000361/2010006-03, "Lack of

preventive maintenance results in valve failure and inoperable condensate

storage tank."

d. Failure to Submit a Licensee Event Report Within 60 Days

Introduction. On April 22, 2010, inspectors identified a Severity Level IV violation

of 10 CFR 50.73, "Licensee Event Report System," in which the licensee failed to

submit a licensee event report within 60 days following failure of condensate

storage tank isolation valve 2HV5715.

Description. As previously discussed, on January 26, 2010, condensate storage

tank T-120 manual isolation valve 2HV5715 failed its in-service stroke test after a

leveraging device was used to turn the hand wheel, at which time it sheared off.

The valve operator stem was heavily rusted and did not move resulting in the

failure. This valve must be closed per San Onofre Procedure AOI S023-13-3,

"Earthquake," Revision 13, Attachment 1, Step 2.3.3 within 90 minutes of an

operating basis earthquake in order to prevent the loss of water inventory from

condensate storage tank T-120 from a line break in the nonseismic portion of the

condensate system.

In determining reportability, an email was attached to Nuclear

Notification 200765235 that stated a mechanic could disassemble the valve

actuator and manually turn the valve. Thus, the licensee concluded the valve

was operable prior to January 26, 2010, and that the failure was not reportable.

The inspectors challenged the use of corrective maintenance to determine that

the valve was previously operable. Originally, licensee representatives informed

the inspectors that its mechanics could pry the position indicator off and close the

valve against the frozen operator using a wrench. The inspectors questioned the

licensee on this position because this action would require turning the stem

against the frozen operator thus potentially damaging the operator.

Following discussions licensee personnel provided a more reasonable position

by stating that the valve operator could be unbolted and removed, and the

butterfly disc stem could then be closed vv;th a ~vvrench. The inspectors

determined this method was plausible, but still required corrective maintenance.

The inspectors noted that the use of corrective maintenance did not meet

- 29- Enclosure 2

NUREG 1022, "Events Reporting Guidelines 10 CFR 50.72 and 50.73," guidance

which states that operability must be ensured and that corrective maintenance is

not an appropriate basis for operability. Tanks T-121 and T-120 are required to

be operable per Technical Specification 3.7.6 to supply 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of

demineralized water to the auxiliary feedwater system. Without the ability to

close valve 2HV5715, tank T-120 was not operable. Because the tank was not

operable, it met the conditions of 10 CFR 50.73(a)(2)(v) as an event or condition

that could have prevented the fulfillment of the safety function of structures or

systems that are needed to shutdown the reactor and maintain it in a safe

shutdown condition, remove residual heat, and mitigate the consequences of an

accident. As such, the event was reportable under 10 CFR 50.73(a)(1).

The licensee maintained its position that based on corrective maintenance the

condition was not reportable until the inspectors pointed out the section in

NUREG 1022, at which time, the licensee determined the condition was

reportable.

The licensee documented this violation in Nuclear Notification 200888616, and

the licensee took actions to issue a licensee event report.

Analysis. The failure to submit a licensee event report as required was a

performance deficiency. The inspectors reviewed this issue in accordance with

Inspection Manual Chapter 0612 and the NRC Enforcement Policy. The

inspectors determined that traditional enforcement was applicable to this issue

because the NRC's regulatory process was impacted. Specifically, the NRC

relies on the licensee to identify and report conditions or events meeting the

criteria specified in regulations in order for the NRC to perform its regulatory

function, and when this is not done, the regulatory function is impacted. The

inspectors determined that this finding was not suitable for evaluation using the

significance determination process, and as such, was evaluated in accordance

with the NRC Enforcement Policy. The finding was reviewed by NRC

management, and the significance of the violation was classified at Severity

Level IV and treated as a noncited violation consistent with the NRC

Enforcement Policy. This finding was determined to have a crosscutting aspect

in the area of human performance in the decision-making component in that the

licensee did not make safety-significant decision using a systematic process,

especially when faced with uncertainty. [H.1 (a)]

Enforcement. Title 10 CFR 50.73(a)(1) requires, in part, that licensees shall

submit a licensee event report for any event of the type described in this

paragraph within 60 days after the discovery of the event. Title 10 CFR 50.73(a)(2)(v) identifies a reportable event as, in part, an event or condition

that could have prevented the fu!fillment of the safety function of structures or

systems that are needed to shutdown the reactor and maintain it in a safe

shutdown condition, remove residual heat, or mitigate the consequences of an

accident. Conti8iY to the above, prior to March 27, 20-10, San Onofre Nuciear

Generating Station failed to submit a licensee event report within 60 days for the

failure of valve 2HV5715 which could have prevented the fulfillment of the safety

- 30 - Enclosure 2

functions and was a condition prohibited by Technical Specification 3.7.6.

Technical Specification 3.7.6 requires that tank T-120 be operable in Modes 1,2,

and 3 in order to supply 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of demineralized water to the auxiliary

feedwater system. Without the ability to close valve 2HV5715, tank T-120 was

not operable. As a result, valve 2HV5715 is a component that is needed to

remove residual heat and mitigate the consequences of an accident. Ail three

trains of auxiliary feedwater could not perform their design function because

there would be insufficient condensate inventory after an earthquake. In

accordance with the NRC's Enforcement Policy, the finding was reviewed by

NRC management and because the violation was of very low safety significance,

and was entered into the corrective action program as Nuclear

Notification 200888616, this violation is being treated as a Severity Level IV

noncited violation, consistent with the NRC Enforcement Policy:

NCV 05000362/2010006-04, "Failure to report conditions that could have

prevented fulfillment of a safety function."

e. Failure by Control Room Operators to Follow Conduct of Operations Procedure

Introduction. The inspectors identified a Green noncited violation of Technical

Specification 5.5.1.1.a, "Scope" for control room operators' failure to adhere to

conduct of operations procedural requirements.

Description. On April 7, 2010, inspectors performed a detailed observation of

control room activities for Units 2 and 3 at San Onofre Nuclear Generation

Station. Unit 2 was performing a startup from a refueling outage and Unit 3 was

operating at 50 percent rated thermal power. The inspectors observed a shift

turnover from night shift to day shift and attended all turnover meetings. The

inspectors watched Unit 2 operators perform startup activities that included a

dilution to within 200 parts per million estimated critical boron concentration.

Additionally, the inspectors observed Unit 2 operators withdraw control rods from

shutdown bank '8' and partial length control rods and viewed Unit 3 operators

perform a dilution with primary water to maintain reactor power at 50 percent.

The inspectors also monitored various routine control room activities such as

acknowledging alarms, refilling the Unit 2 closed cooling water surge tank, and

controlling pressure in the Unit 2 steam generators. The inspectors observed the

control room operators interacting with other departments such as maintenance,

health physics, engineering, and chemistry.

The inspectors compared actions in the control room with San Onofre

Procedure S0123-0-A 1, "Conduct of Operations," Revision 26, and observed

numerous deficiencies. When Unit 2 alarms were received in the control room,

the inspectors observed the following:

.. Place keeping was not implemented on any unexpected alarms received

in the Unit 2 control room per Section 6.4.3.3 and Guideline 5 of

Section 6.'1.3. ,i\!arm response procedures 'vVere refeired to by the reactor

operators and read but no place keeping occurred.

- 31 - Enclosure 2

The operator announcing the alarm did not always report it to the control

room supervisor as required by Section 6.4.3.3.

When an alarm annunciated, or an alarm condition clears, all

conversations in the control room did not stop until the alarm had been

acknowledged or reset, as required by Section 6.4.3.1.

The following alarms were received in the Unit 2 control room during the

inspectors' observations:

  • Generator potential transformer fuse blown
  • Channel 4 startup rate high
  • Control Element Assembly Group Deviation (the senior reactor operator

in charge of reactivity instructed the reactor operator to mark steps in

alarm response procedure)

  • Other alarms were received during the observation but marking of alarm

response procedures were not normally performed

The inspectors observed a control room supervisor conduct a pre-job briefing at

the beginning of shift. During the briefing, numerous questions were asked of the

control room supervisor by on-shift operators on how the supervisor wanted the

operators to control steam generator pressure. The questions or answers were

not acknowledged using three-way communications to ensure full understanding

took place as required by Section 6.6.4.7 of San Onofre Procedure S0123-0-A 1.

Throughout the inspector's observations, additional examples of missed three

way communications were observed.

In addition, when an operator was performing the filling of the closed cooling

water surge tank, the operator did not verify written instruction prerequisites

before using the procedure as required by San Onofre Procedure S0123-0-A 1.

During the pre-job brief for pulling shutdown group '8' and partial length control

rod groups, the reactivity senior reactor operator did not verbalize the five

summarize, anticipate, foresee, evaluate and review questions as part of the

brief. Only the operating experience question was discussed. Other items not

reviewed as required included: (1) four questions dealing with critical steps,

(2) error-likely situations, (3) how bad can it get, and (4) what defenses are in

place and are they adequate. These were required by San Onofre

Procedure S0123-0-A 1.

During a Unit 3 reactivity change, the inspectors obsented the contre! room

supervisor performing oversight of the activity take a phone call while the

evolution was in progress. The control room supervisor first engaged in

- 32 - Enclosure 2

conversation before informing the person that he would have to call them back

later. This was contrary to Section 6.5.2, Step 6.5.2.8 which states, "All reactivity

changes in the control room require direct senior reactor operator oversight.

Senior reactor operator oversight requires the senior reactor operator be

cognitive of, present for, and approve the reactivity change."

The licensee documented these procedural deficiencies in Nuclear

Notification 200871332 and its short term corrective actions included operation's

management reviewing the observations with the inspectors and then

establishing a recovery plan to improve operator performance.

Analysis. The failure of control room operators to adhere to conduct of

operations procedural requirements is a performance deficiency. The finding

was more than minor because, uncorrected, the failure to follow these procedural

requirements could lead to a significant safety concern due to the potential of

operators making errors while operating safety-related systems. Using the

Inspection Manual Chapter 0609, "Significance Determination Process," Phase 1

Worksheet, the inspectors determined the finding had a very low safety

significance because the finding did not result in a loss of system safety function,

an actual loss of safety function of a single train for greater than its technical

specification allowed outage time, or screen as potentially risk significant due to a

seismic, flooding, or severe weather initiating event. As a result, the issue was of

very low safety significance (Green). The finding has a crosscutting aspect in the

area of human performance associated with the work practices because the

licensee did not ensure supervisory and management oversight of work activities.

H.4(c)

Enforcement. Technical Specification 5.5.1.1.a, "Scope" requires, in part, that

written procedures be established, implemented, and maintained covering the

activities specified in Appendix A, "Typical Procedures for Pressurized Water

Reactors and Boiling Water Reactors," of Regulatory Guide 1.33, "Quality

Assurance Program Requirements (Operations)," dated February 1978.

Specifically Regulatory Guide 1.33 Section 1.d "Procedure Adherence," requires

operators to follow their procedures. San Onofre Procedure S0123-0-A 1,

"Conduct of Operations," Revision 26, Sections 6.4.3.1,6.6.4, and 6.5.2 require,

in part, the following: implement alarm response procedure place keeping;

announce alarms to the control room supervisor; stop conversations in the

control room when an alarm annunciates; perform 3-way communications during

pre-job briefing; review the five questions, summarize, anticipate, foresee,

evaluate and review, during a pre-job brief; and review the prerequisites prior to

each use of a procedure; and requires that a senior reactor operator remain

cognitive of the reactivity change evolution.

Contrary to this, on April 7, 2010, control room operators failed to follow San

Onofre Procedure S0123-0-A 1, "Conduct of Operations," Revision 26,

requirements in numerous instances including fai(ui6s to: implenlent c3;arrn

response procedure place keeping; announce alarms to the control room

supervisor; stop conversations in the control room when an alarm annunciated;

- 33- Enclosure 2

perform 3-way communications during a pre-job briefing; review the five

questions, summarize, anticipate, foresee, evaluate and review, during a pre-job

brief; review the prerequisites prior to each use of a procedure; and remain

cognitive of the reactivity change evolution by a control room supervisor.

Because this finding is of very low safety significance and has been entered into

the licensee's corrective action program as Nuclear Notification 200871332, this

violation is being treated as a noncited violation, consistent with Section VI.A of

the NRC Enforcement Policy: 05000362/2010006-05; "Control Room Operators'

Failure to Adhere to Conduct of Operations Procedural Requirements."

f. Failure to Provide Adequate Procedures for Boron Dilution Activities

Introduction. The inspectors reviewed a self-revealing Green noncited violation

of Technical Specification 5.5.1.1.a, "Scope" for the failure of boron saturation

procedure to have adequate direction to prevent an unplanned power transient

Description. On December 25, 2009, the chemistry department requested

operators to perform a reactor coolant system delithiation using ion

exchanger 3ME074 for Unit 3. This ion exchanger was not boron saturated so

the evolution would require diverting to radiological waste while performing a

manual blended makeup.

The operating crew performed a pre-job brief prior to commencing the evolution

where they discussed the procedures, expected plant response, and

compensatory actions for power increase. The crew reviewed the logs and found

the last blended makeup to be light in boron concentration which could result in a

slight power increase. The crew was aware of Unit 3 having a feedwater heater

leak that was identified on the previous shift. The leak was scheduled to be

repaired later that day and would require a slight down power to remove the

feedwater heater from service. The crew was concerned with exceeding the

licensed power limit and therefore set an upper power limit of plus 0.5 percent.

Due to a down power scheduled later that day the crew did not set a lower power

limit nor did they believe it was required.

San Onofre Procedure S023-3-2.4,controlling the evolution, "RCS Purification

and De-borating Ion Exchanger Operation," Revision 21, provided a guideline to

stop the evolution at 10 minutes for the crew to monitor plant response to

determine if it was as expected. The crew believed that the blended makeup

would be light and plant response was known.

The crew commenced the evolution to boron-saturate the ion

exchanger 3ME074. However, the crew did not stop the evolution at 10 minutes

because they did not believe it to be a requirement. As a result, the crew over-

borated the reactor and caused an unplanned down power of 0.74 percent.

Operation management conducted an investigation of the event and initiated a

Nuclear Notification 200721702. The crew members involved in the event were

coached about expected performance during reactivity manipulations.

- 34- Enclosure 2

Operations issued a priority 2 notification to the operations department describing

the event and management's expectations for reactivity activities. San Onofre

Procedure S023-3-2.4 was revised to place procedure requirements in place to

prevent events such as this from occurring again.

Analysis. The failure to have adequate procedural direction to control plant

power changes is a performance deficiency. The finding was more than minor

because it was associated with the initiating events cornerstone attribute of

human performance, and it affected the associated cornerstone objective to limit

the likelihood of those events that upset piant stabiiity and that challenge critical

safety functions during shutdown, as well as during power operations. Using the

Inspection Manual Chapter 0609, "Significance Determination Process," Phase 1

Worksheet, the inspectors concluded that the transient initiator did not contribute

to both the likelihood of a reactor trip and to the likelihood that mitigation

equipment or functions would not be available. As a result, the issue was of very

low safety significance (Green). The finding has a crosscutting aspect in the

area of human performance associated with the work practices because licensee

supervisory personnel did not ensure activities associated with reactivity control

were performed in a controlled manner such that nuclear safety was assured.

H.4(c)

Enforcement. Technical Specification 5.5.1.1.a requires, in part, that written

procedures be established, implemented, and maintained covering the activities

specified in Appendix A, "Typical Procedures for Pressurized Water Reactors

and Boiling Water Reactors," of Regulatory Guide 1.33, "Quality Assurance

Program Requirements (Operations)," dated February 1978. Specifically

Regulatory Guide 1.33 section 3.n "Chemical and Volume Control System," shall

have instructions for controlling power changes. Contrary to this, as of

December 25, 2009, San Onofre Procedure S023-3-2.4, "RCS Purification and

De-borating Ion Exchanger Operation," Revision 21, was inadequate in that it

only provided guidelines, not requirements, to control the borating of ion

exchangers. As a result, an operations crew performed the evolution and did not

adhere to guidelines (because they were not required) and over-borated the

reactor, which in turn caused an unplanned down power transient of

0.74 percent. Because this finding is of very low safety significance and has

been entered into the licensee's corrective action program as Nuclear

Notification 200721702, this violation is being treated as a noncited violation,

consistent with Section VI.A of the NRC Enforcement Policy: 05000362/2010006-

06, "Failure to provide adequate procedure for boron dilution activities."

g. Inadequate Procedures for Radiation Monitoring of Component Cooling Water

Introduction. The inspectors identified a noncited violation of Technical

Specification 5.5.1.1.a, "Scope," involving the failure to establish procedures for

component cooling water system alignments such that leakage of radionuclides

to the environment would be monitored during all operational alignments of

component cooling water. Specifically, radiation monitors could be aligned to

only one train of component cooling water at a time and the licensees'

- 35 - Enclosure 2

procedures had no provision for monitoring the second train when both trains

were in-service.

Description. On April 5, 2010, inspectors walked down the component cooling

water system during which San Onofre Nuclear Generating Station personnel

discussed heat exchanger tube leakage in the Unit 2 train B heat exchanger

below the operability limit of 18 gallons per minute. The surge tank level was

decreasing and component cooling water inventory was being lost to the salt

water system. The salt water system is the ultimate heat sink for safety

equipment and it operates at a lower pressure than component cooling water.

Inspectors reviewed the current operability evaluation contained in Nuclear

Notification 200823240 as well as system piping and instrumentation drawings,

and learned that radiation monitor 7819 (Unit 2 and Unit 3) can only be aligned to

one train of component cooling water at a time. That is because it is connected

to the non-critical loop. Noncritical loop loads include the radioactive waste

building and containment loads such as control rod drive mechanism cooling and

reactor coolant pump cooling. Leakage from the shutdown cooling heat

exchangers would be captured by the component cooling water system but the

radioactivity may not be measured depending on which train of component

cooling water is aligned to radiation monitor 7819.

Inspectors reviewed Final Safety Analysis Report, Section 9.2.2.1 and found that

the component cooling water system is designed to be an intermediate barrier

between salt water and contaminated heat loads during non-accident scenarios.

Final Safety Analysis Report Section 11.5.2.1.3.1 describes radiation

monitor 7819 on the non-critical loop: "The component cooling water monitor

samples component cooling water from a noncritical component cooling water

line that may be isolated from the rest of the component cooling water for certain

engineered safety features actuation system conditions. Whenever the

noncritical loop of component cooling water is isolated, the system is not

monitored and in-leakage to the component cooling water from a higher activity

system will not be detected." The Final Safety Analysis Report states that

component cooling water is operated at a higher pressure than salt water. This

also causes a potential release path.

The alignment of the noncritical loop radiation monitor described in

Section 9.2.2.2.1 of the Final Safety Analysis Report was not in accordance with

procedures. San Onofre Procedure S023-2-17, "Component Cooing Water

System Operation," Revision 32, Step 6.7 and Attachment 9 Step 6.2 did not

direct operators to align the letdown heat exchanger to the component cooling

water loop being monitored by radiation monitor 7819 or direct compensatory

radiation monitoring by other means. The steps leave this part of system

alignment to the discretion of the operator. In addition, plant operators did not

question the procedure's adequacy when both trains of component cooling water

were in service.

The inspectors concluded that the licensing basis was not correctly implemented

with this procedure. San Onofre Procedure AOI S023-13-7, "Loss of Component

- 36- Enclosure 2

Cooling Water (CCW)/Saltwater Cooling (SWC)," Revision 14 (EC 14-1),

Step 13.e, directed operators to check that the trend on radiation monitor 7819

was normal when system leakage is detected. Inspectors found that this was not

in accordance with Final Safety Analysis Report, Section 9.2.2.3.2. The steps

contained instructions to check the radiation monitor trend but not to ensure that

it was aligned to the train that was suspected of leakage.

The inspectors found that San Onofre Nuclear Generating Station did not

translate the component cooling water system design into procedures that

ensured that radionuclide releases would not occur without monitoring in all

operational alignments. Radiation monitor 7819 is not in the Offsite Dose

Calculation Manual as a release point. Final Safety Analysis Report

Section 11.5.1.2, Effluent Monitoring Systems, does not describe the component

cooling water system as a monitored release point or radiation monitor 7819 as

an effluent radiation monitor. Plant procedures and sections of the Final Safety

Analysis Report support general design criterion 64 for monitoring of radioactive

releases.

Inspectors concluded that San Onofre Nuclear Generating Station did not

consider the component cooling water system heat exchangers as release paths

in several alignments such as shutdown cooling, emergency core cooling system

sump recirculation, normal chemical and volume control system letdown, and

spent fuel cooling. Plant procedures contained no consideration that component

cooling water radiation monitors 7819 (Unit 2 and Unit 3) could only be aligned to

one train of component cooling water at a time but that in-leakage could

potentially occur in the opposite component cooling water train and be released

to the salt water system. Although monthly grab sample monitor component

cooling water, this frequency is not sufficient to monitor for radionuclides which

could be released into Salt Water Cooling. As a result, existing procedures to

monitor component cooling water leakage while at power were inadequate to

ensure grab sampling of the component cooling water train not aligned to

radiation monitor 7819 (Unit 2 and Unit 3).

The licensee entered this issue into the corrective action program as Nuclear

Notification 200871387, and instituted compensatory actions to routinely sample

the component cooling water train that is not aligned to the radiation monitor and

to perform sampling when the radiation monitor is not in service. These

compensatory measures are to remain in place until San Onofre Nuclear

Generating Station completes its evaluation of the issue.

Analysis. The failure to translate the design bases into procedures that ensure

the radiation monitoring of the safety-related component cooling water system in

all operational alignments is a performance deficiency. The inspectors

determined that this finding was more than minor because this issue impacted

the Public Radiation Protection Cornerstone and its objective to ensure adequate

protection of public health and safety from exposure to radioactive mateiials

released into the public domain as a result of routine civilian nuclear reactor

operation. Specifically, the component cooling water radiation monitors were not

- 37 - Enclosure 2

sufficient to ensure adequate release measurements. The inspectors evaluated

the significance of this finding using Phase 1 of Inspection Manual

Chapter 0609.04 and determined that the finding screened to Inspection Manual

Chapter 0609, Appendix D, Public Radiation Safety Significance Determination

Process. The inspectors evaluated the significance of this finding using

Inspection Manual Chapter 0609, Appendix D, and determined that the finding

was of very low safety significance because dose did not exceed Appendix I

criteria. This finding was determined to have a crosscutting aspect in the area of

problem identification and resolution associated with the corrective action

program in that plant operators did not have a low threshold for identifying

deficiencies in procedures. [P.1 (c)]

Enforcement. Technical Specification 5.5.1.1.a. requires, in part, that written

procedures be established, implemented, and maintained covering the activities

specified in Appendix A, "Typical Procedures for Pressurized Water Reactors

and BOiling Water Reactors," of Regulatory Guide 1.33, "Quality Assurance

Program Requirements (Operations)," dated February 1978; Section 7.g requires

procedures for radiation monitoring operation. Contrary to the above, prior to

April 22, 2010, the licensee failed to establish procedures for component cooling

water system alignments that would prevent unmonitored leakage to the

environment through leakage into the Salt Water Cooling system. Because the

violation was of very low safety significance and was entered into the corrective

action program as Nuclear Notification 200871387, this violation is being treated

as noncited violation, consistent with the NRC Enforcement Policy VI.A:

NCV 05000361/2010006-07, "Failure to Establish Component Cooling Water

Radiation Monitoring Procedures."

h. Failure to Revise Procedures with Known Technical Errors

Introduction. The inspectors identified a cited violation of Technical

Specification 5.5.1.1 a for the failure to maintain written procedures covered in

Regulatory Guide 1.33. Specifically, as of April 2010, the licensee failed to

properly control procedure changes associated with plant modifications resulting

in procedures with known technical deficiencies being used at the facility.

Description. On April 8, 2010, the inspectors reviewed corrective actions from

two previous noncited violations for the licensee's failure to maintain procedures.

The first noncited violation was 05000361 :05000362/2009003-02 and was

associated with the licensee's failure to implement controls over its backlog of

procedure change requests such that procedures with known technical

deficiencies were in use in the field (before being revised). The second noncited

violation was 05000361 :05000362/2009009-02 and also involved the licensee's

failure to implement controls over its backlog of procedure change requests such

that procedures with known technical deficiencies were in use in the field.

During this inspection, the inspectors identified that the backlog of procedure

change requests had increased to 3,389. The inspectors identified that most of

these procedure changes were appropriately classified according to the "TEAM"

- 38- Enclosure 2

method in accordance with San Onofre Procedure S023-XV-1 09.1, "Procedure

Action Request Committee Process," Revision 1. The inspectors approach

classifies procedure changes as technical, enhancement, administrative

correction, or modification. Technical changes were defined for plant impacting

procedures or procedures that must be issued the next business day as changes

that could place a structure system or component in an unevaluated condition;

could cause a plant trip; could cause a loss of megawatts; could degrade nuclear

safety; could cause unexpected reactivity changes; or could cause an immediate

personnel safety issue. However, for procedure changes related to plant

modifications the inspectors identified that there was no procedural direction to

ensure technical procedure changes were incorporated for operating the

equipment following modifications. Additionally, the inspectors identified at least

one procedure change request that had been inappropriately classified as a plant

modification when it was, in fact, a technical procedure change that was

unrelated to a plant modification. (see Section 40A2.51)

The inspectors requested that the licensee review the backlog of modification-

related procedure changes to determine if any were related to modifications that

had already been installed in the plant. Of the 212 modification-related

procedure changes in the backlog, the licensee identified 60 procedure changes

associated with plant modifications that were either installed or partially installed.

These 60 pending changes included changes to 10 procedures, including one

alarm response procedure, associated with a modification to the instrument air

system which had been installed during Unit 2 refueling outage R2C16; these

procedures did not reflect the current plant configuration. Following the

inspectors' identification of these unincorporated technical changes, the licensee

initiated a full review of plant modifications classified procedure change requests.

The licensee identified a total of 18 procedures which required technical changes

as a result of plant modifications. The licensee agreed that these procedure

changes should have been made prior to the associated plant modifications

being turned over to operations. The result had been that procedures with

known technical deficiencies as a result of plant modifications had been in use in

the field.

The inspectors further identified that the process for ensuring modification-related

procedure changes were incorporated prior to the modifications being turned

over to operations was informal and was not controlled by procedure. The

determination of which procedure changes were important and which could be

deferred was left up to the procedure writer; there was no procedural guidance

for making this determination. This finding was entered into the licensee's

corrective action program as Nuclear Notification 200888919, and the licensee

took actions to suspend use of the affected procedures until they could be

revised.

Analysis. The failure to maintain San Onofre Nuclear Generator Station

procedures covered by Regu!atory Guide 1.33 is a performance deficiency. The

finding is of more than minor significance because, if left uncorrected, it would

have the potential to lead to a more significant safety concern by having

- 39- Enclosure 2

technically inaccurate procedures being used on important plant systems. Using

Inspection Manual Chapter 0609.04, Phase 1 "Initial Screening and

Characterization of Findings," the finding was determined to have a very low

safety significance because the finding did not result in a loss of system safety

function, an actual loss of safety function of a single train for greater than its

technical specification allowed outage time, or screen as potentially risk

significant due to a seismic, flooding, or severe weather initiating event. The

finding has a crosscutting aspect in the area of problem identification and

resolution associated with the corrective action program component because

problems were not thoroughly evaluated such that the resolutions addressed the

causes and extents of condition. [P.1 (c)]

Enforcement. Technical Specification 5.5.1.1.a requires, in part, that written

procedures be established, implemented, and maintained covering the applicable

procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A,

February 1978. Regulatory Guide 1.33, "Quality Assurance Program

Requirements (Operations)," Appendix A, recommends procedures for the

operation of certain plant systems. Contrary to the above, as of April 2009, the

licensee failed to maintain written procedures as recommended in Regulatory

Guide 1.33, Revision 2, Appendix A, February 1978. Specifically, the licensee

did not ensure that following equipment modifications made to the instrument air

system, procedures requiring technical changes were suspended, put on

administrative hold, or otherwise restricted from use until the required changes

were made. As a result, severa! procedures with known technical deficiencies

were available for operator use.

This performance deficiency was previously identified by the NRC on two

occasions and were documented as noncited violations 05000361:

05000362/2009003-09 and 05000361;05000362/2009009-02. The inspectors

determined that the licensee had failed to restore compliance within a reasonable

time following issuance of these noncited violations. Therefore, this violation is

being cited in a Notice of Violation consistent with Section VI.A of the NRC

Enforcement Policy: VIO 05000361;05000362/2010006-08, "Failure to Maintain

Written Procedures Covered in Regulatory Guide 1.33."

i. Failure to Set Goals In Accordance With the Maintenance Rule

Introduction. The inspectors identified two examples of a Green noncited

violation of 10 CFR 50.65(a)(2) for failure to monitor the performance of auxiliary

feedwater system components against established goals in a manner to provide

reasonable assurance that the system was capable of fulfilling designated

auxiliary feedwater maintenance rule functions.

Description. Under the maintenance rule, San Onofre Nuclear Generating

Station defines three separate functions for monitoring the auxiliary feedwater

system. Function 1 has a stated purpose fOi motor-driven Train A to supply

feedwater from the condensate feedwater tanks to steam generator 88 for plant

cool down when main feedwater is unavailable. Function 2 is identical except

- 40- Enclosure 2

that it tracks motor-driven Train B auxiliary feedwater. Function 3 covers the

turbine-driven auxiliary feedwater pump to supply both steam generators. All

three functions stated that they include the water supply piping and valves from

condensate storage Tanks T -120 and T-121. The auxiliary feedwater system

has unavailability goals of 1.2 percent per 12 month period for functions 1 and 2

and 1.1 percent per 12 month period for function 3. This equates to

approximately 79.3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> of unavailability for function 3.

On December 9, 2008, San Onofre Nuclear Generating Station performed flawed

maintenance that bent the fuse holder contacts such that there was a loose

electrical connection. On December 19, 2008, the control room received an

annunciator indicating a problem with the Unit 3 turbine driven auxiliary

feedwater pump. The licensee identified the loose electrical connection caused

the alarm and repaired the connection early on December 20, 2008. In Nuclear

Notification 200253911, the licensee counted 9.6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> of unavailability because

that was the time from control room annunciation of a problem to the completion

of repairs. The maintenance rule evaluation did not elaborate as to why this

amount of time was used. The inspectors noted that the ioose connection

existed for approximately 10 days prior and for approximately 64 hours7.407407e-4 days <br />0.0178 hours <br />1.058201e-4 weeks <br />2.4352e-5 months <br /> while

Unit 3 was in Mode 1.

When questioned by the inspectors, San Onofre Nuclear Generating Station

personnel stated the basis for using 9.6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> was that the pump was functional

because only its earthquake qualification was in question. Inspectors found that

the evaluation of the loose connection did not consider resistance heating of the

loose connection or that an earthquake was not required for the failure to be

annunciated in the control room. The counting of additional unavailability hours

would have caused the Unit 3 turbine driven auxiliary feedwater pump to exceed

its 10 CFR 50.65 (a)(2) goal and be placed into (a)(1) status. However, since the

pump had been previously placed in (a)(1) status in April 2009 due to functional

failures, the approximately 64 hours7.407407e-4 days <br />0.0178 hours <br />1.058201e-4 weeks <br />2.4352e-5 months <br /> additional hours of unavailability would have

prevented the system from transitioning back to (a)(2) status within 6 months.

When questioned, plant personnel informed the inspectors that it utilized NRC

performance indicator guidance from NEI 99-02 as its evaluation of unavailability.

Combined with other system unavailability, function 3 would exceed its

approximately 80 hour9.259259e-4 days <br />0.0222 hours <br />1.322751e-4 weeks <br />3.044e-5 months <br /> unavailability monitoring goal and (a)(1) monitoring would

have been significantly extended. Because the licensee performed an

inadequate evaluation of unavailability time, the system was returned to (a)(2)

status on August 20, 2009.

The second example of inadequate evaluation of unavailability time involved the

licensee's maintenance rule evaluation of the failure of auxiliary feedwater

condensate isolation valve 2HV5715. On January 26, 2010, valve 2HV5715

failed its in-service stroke test (as described in section 40A2.5c). The hand

wheel stem snapped when a leveraging device was used to attempt to open the

valve. The valve operator stem \lJaS heavily rusted because it had been i6moved

from the preventive maintenance regimen program. This valve must be closed

per procedure within 90 minutes of an Operating Basis Earthquake to prevent the

- 41 - Enclosure 2

loss of water inventory from condensate storage tank T -120 from a line break in

the non-seismic portion of the condensate system. Nuclear

Notification 200765235 was written to evaluate the broken valve.

Inspectors found that the maintenance rule evaluation counted a functional

failure for the valve, but utilized Mitigating Systems Performance Index guidance

from NEI 99-02 for unavailability. Inspectors found that use of this guidance was

inappropriate to the circumstances and that the evaluation was inadequate. The

licensee also utilized Appendix C to NRC Inspection Procedure 71111.13 for

evaluating unavailability time, but only considered limited portions of the

guidance. The licensee's program procedure described availability but did not

provide sufficient guidance for this situation.

The maintenance rule evaluation in Nuclear Notification 200765235 also stated

that since the valve failed its stroke test in Mode 6, that there was no

unavailability impact. The evaluation stated: "The timing of when this valve

would no longer close is unknown and may have been during the required

Mode 1 thru 3." inspectors found that the iicensee had not attempted to perform

an engineering evaluation to determine when the valve failed due to the rust.

Given the as-found condition, the number of unavailability hours was most likely

significantly higher than the 79 hour9.143519e-4 days <br />0.0219 hours <br />1.306217e-4 weeks <br />3.00595e-5 months <br /> monitoring threshold. This long-standing

deficiency was significant because no preventive maintenance had been

performed on the valve resulting in its degradation. This deficiency impacted all

three maintenance rule functions for the auxiliary feedwater system.

Step 6.5.1.7 of San Onofre Procedure S0123-XV-5.3, "Maintenance Rule

Program," required the monitoring of unavailability for these trains. Due to

inadequate tracking and accounting, the licensee failed to identify that it

exceeded the auxiliary feedwater trains' monitoring goal. San Onofre

Procedure S0123-XV-5.3, Step 6.5.1.7, required review of functional

unavailability information from all sources as necessary to ascertain performance

relative to established criteria. Lastly, San Onofre Procedure S0123-XV-5.3,

Step 6.5.1.7, required that when a trend of performance indicates a performance

criterion has been exceeded, the train will be evaluated for goal setting. This did

not occur. As a result, the plant engineering department took action to evaluate

the issues identified by the inspectors and is reviewing existing guidance. These

actions were documented in Nuclear Notification 201001922.

Analysis. Failure to adequately account for unavailability time in the licensee's

maintenance rule evaluation of the auxiliary feedwater system is a performance

deficiency. This finding is more than minor because it affects the equipment

performance attribute of the Mitigating Systems Cornerstone per Inspection

Manual Chapter 612, Appendix B. Specifically, San Onofre Nuclear Generator

Station failed to appropriately account for system unavailability hours which

would have resulted in the moving the system to (a)(1), requiring goals and

........"" ..... i+_r;-...... _ +h ___ r+_ ... ..--. _______ ;_ .... 4- ... L-.. ______ I .... ,c_ .... +L-.. ........ L.. ... __ ..... , ... ..,:I: __ ~. & __ -.1 *** _.&._-

IIIVIII'V'~ l I l v ,",vIIVI' llal ,,",v a~alll;:)l LlIV;:)t; l::Ival;:) IVI LIlt; Llil t;t; ClUAIIiClI Y IttUVVClttl

functions. The inspectors evaluated the significance of this finding using

Inspection Manual Chapter 0609.04, Phase 1 "Initial Screening and

- 42- Enclosure 2

Characterization of Findings," and determined that this finding is of very low

safety significance, Green. Specifically, the maintenance rule is an

administrative activity that could not result in the loss of a system safety function,

an actual loss of safety function of a single train for greater than its technical

specification allowed outage time, or screen as potentially risk significant due to a

seismic, flooding, or severe weather initiating event. The cause of the finding

was determined to have a crosscutting aspect in the area of human performance

in the decision-making component because the licensee did not use a systematic

process when faced with the unexpected unavailability for the latent equipment

deficiencies. H.1.a]

Enforcement. Title 10 CFR 50.65 requires, in part, when performance of

systems, structures, or components cannot be demonstrated per paragraph

(a)(2), that performance goals and corrective action shall be established under

paragraph a(1). San Onofre Nuclear Generating Station's monitors auxiliary

feedwater maintenance rule functions 1, 2, and 3 with an unavailability goal of

approximately 80 hours9.259259e-4 days <br />0.0222 hours <br />1.322751e-4 weeks <br />3.044e-5 months <br /> per rolling 12 month period. Contrary to the above, on

January 26, 2009, and December 9, 2008, San Onofre Nuclear Generator

Station's auxiliary feedwater maintenance rule functions 1, 2, and 3 exceeded

their (a)(2) monitoring goals and San Onofre Nuclear Generator Station failed to

evaluate and establish (a)(1) goals. Specifically, the evaluations discounted

significant unavailability hours from long maintenance induced failures that would

have cause the 80 hour9.259259e-4 days <br />0.0222 hours <br />1.322751e-4 weeks <br />3.044e-5 months <br /> goals to be exceeded. Because this violation was of

very low safety significance and was entered into the licensee's corrective action

program under Nuclear Notification 201001922, this violation is being treated as

a noncited violation in accordance with the NRC Enforcement policy:

NCV 05000361/05000362/2010006-09, "Failure to Establish Goals and Monitor

for a(1) auxiliary feedwater trains."

j. Failure to Identify and Correct the Use of Degraded Relays in Safety-Related

Equipment

Introduction. The inspectors identified a Green noncited violation of

10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," for the licensee's

failure to promptly identify and correct conditions adverse to quality. Specifically,

the licensee performed an inadequate extent of condition review and failed to

identify that deficient motor driven rotary relays were installed in various safety-

related applications.

Description. On August 5,2007, the Unit 3 emergency diesel generator 3G002

was taken out of service for preventive maintenance. On August 9,2007, the

licensee performed preventive maintenance in the emergency diesel generator

cabinet 3L 160. The maintenance activity instructs personnel to perform continuity

checks for all associated contacts in the electrical cabinet to ensure they are in

the correct position, and then perform relay checks to ensure the relays and

associated contacts peiform as expected when energized or de-energized.

During performance of the maintenance activity, maintenance personnel reported

(Action Request 070800466) that normally de-energized relay 3L 160-2-K52, a

- 43- Enclosure 2

Potter & Brumfield motor driven relay, was sluggish and would not rotate

completely. The 2008 problem identification and resolution team documented

the deficiency in NCV 05000362/2008012-02, "Failure to Properly Implement

Operability Determination Process" because the licensee did not perform an

operability determination of the sluggish relay. The licensee entered the issue

into the corrective action program as Nuclear Notification 200146292.

The licensee evaluated the motor driven relays in Direct Cause

Evaluation 8001654561, and determined that the cause of the failure was an

oversized coil manufacturing deficiency. The licensee stated that this was a "well

documented failure mechanism for Potter & Brumfield motor driven relays

manufactured between 1989 and 1992." The licensee also stated that "there are

a large number of normally de-energized motor driven relays in the plant from the

manufacturing lots with the oversize coils." The licensee replaced the relays,

whose failure could impact the operability of the emergency diesel generators,

with new relays that were manufactured with a retaining ring around the coil to

prevent oversized coil failures. The licensee generated Nuclear

Notification 200188863 to address the extent of condition. However, the extent

of condition only focused on the motor driven relays installed in the four

emergency diesel generators.

The inspectors asked if the deficient motor driven relays, which remained

installed in the plant and were not covered in the scope of the extent of condition

review, were installed in safety-related applications. The licensee found 62

normally de-energized relays whose failure "could impact the performance of a

specified safety function." The licensee generated Nuclear

Notification 200887995 and created maintenance orders to replace the degraded

relays at the next available opportunity.

Analysis. The failure to perform an adequate extent of condition evaluation and

identify and correct a condition adverse to quality was a performance deficiency.

This finding was more than minor because it impacted the equipment

performance attribute of the Mitigating Systems Cornerstone objective to ensure

the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. Using Inspection Manual

Chapter 0609.04, Phase 1 ,"Initial Screening and Characterization of Findings,"

the inspectors determined the finding to be of very low safety significance

(Green) because it did not represent the loss of a system safety function and did

not screen as potentially risk significant due to a seismic, flooding, or severe

weather initiating event. This finding has a crosscutting aspect in the area of

human performance associated with the decision-making component in that the

licensee did not use conservative assumptions in making decisions about the

extent of condition. [H.i (b)]

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective

Action/' requires, in part, that measures sha!! be established to assure that

conditions adverse to quality are promptly identified and corrected. Contrary to

the above, from October 2008, to April 2010, the licensee did not promptly

- 44- Enclosure 2

identify and correct the use of deficient motor driven relays in safety-related

systems and components. Because the finding is of very low safety significance

and has been entered into the corrective action program as Nuclear

Notification 200146292, this violation is being treated as a noncited violation

consistent with Section VLA of the NRC Enforcement Policy: NCV 05000361;05000362/2010006-10, "Failure to Identify and Correct Use of Deficient Motor

Driven Relays."

k. Failure to Secure Loose Items in the Switchvard

Introduction: A Green noncited violation of Technical Specification 5.5.1.1.a was

identified involving the failure to follow San Onofre Procedure S0123-XX-11,

"Switchyard Work Performance" Revision 2. Specifically, the inspectors

identified the licensee's faiiure to adequately control loose material within the

switchyard.

Description: On April 7, 2010, inspectors performed a walkdown of the 230kV

switchyard. During the walkdown, inspectors identified several pieces of

temporai)' moveable equipment that were not tethered in the switchyard.

Inspectors determined that loose material in the switchyard could be hazardous

to electrical equipment that could affect the loss of offsite power in the event of

seismic activity, tornados, high winds, or hurricanes. The licensee entered a

Nuclear Notification 200870138 in their corrective action program to evaluate the

condition. The licensee's San Onofre Procedure S0123-XX-11 "Switchyard

Work Performance" Revision 2, under Section 6.12, "Temporary Equipment",

Step 6.12.1, specifically states, "All unattended temporary movable equipment

left in the Switchyard or Relay House SHALL be restrained in such a manner so

as to prevent damage to any installed equipment during a seismic event."

The inspectors interviewed plant personnel and determined that personnel failed

to remove the materials from the switchyard subsequent to completing assigned

work activities in the switchyard. The licensee verified that three of the loose

items found by inspectors had been in the switchyard unrestrained since the first

week of October 2009, three other items had been unrestrained in the switchyard

since March 2, 2010, and two more items had been unrestrained in the

switch yard for the life of the plant. The licensee failed to provide effective

oversight to ensure the loose material was tied down throughout the duration of

work being performed in the switchyard as well as the removal of material

following completion of the respective jobs.

The licensee documented this violation in Nuclear Notification 200870138, and

its short term corrective actions included removing or securing loose items,

evaluating materials in the switchyard for high winds and seismic concerns, and

ensuring operator rounds that included checking for loose material.

Analysis. The failuie to contiOl loose material near risk-significant equipment is a

performance deficiency. This finding is more than minor because it impacts the

protection against the external factors attribute of the Initiating Events

- 45- Enclosure 2

Cornerstone objective to limit the likelihood of those events that upset plant

stability and challenge critical safety functions during shutdown and power

operations. Using the Significance Determination Process Phase 1 worksheets

from Inspection Manual Chapter 0609, the inspectors determined that the finding

was of very low safety significance (Green) because it did not contribute to both

the likelihood of a reactor trip and the likelihood that mitigation equipment or

functions would not be available. This finding also has a human performance

crosscutting aspect associated with the work control component in that personnel

failed to appropriately plan work activities involving job site conditions which may

impact plant structures, systems and components. H.3(a)

Enforcement. Technical Specification 5.5.1.1.a, in part, requires that procedures

be established, implemented, and maintained covering the applicable procedures

in Regulatory Guide 1.33, Appendix A. Regulatory Guide 1.33, Appendix A,

requires in part, written procedures for Acts of Nature (e.g. tornado, flood, dam

failure, earthquakes). Contrary to the above, the licensee failed to follow

procedure as required by Regulatory Guide 1.33, Appendix A. Specifically, the

licensee failed to adequately control loose material in the switchyard as required

by San Onofre Procedure S0123-XX-11, "Switchyard Work Performance,"

Revision 2. The licensee entered a notification in their corrective action program

as Nuclear Notification 200870138. This violation is being treated as a noncited

violation, consistent with Section Vela of the Enforcement Policy:

NCV 05000361;05000362/2010006-11, "Failure to control loose items in the

electrical switchyard."

I. Failure to Translate Design Basis Information into Affected Calculations and

Procedures

Introduction. The inspectors identified two examples of a noncited violation of

10 CFR Part 50, Appendix B, Criterion III, "Design Control," for the failure of the

licensee to ensure that new information affecting the plant design bases was

incorporated into affected procedures, calculations, and drawings. Specifically,

the inspectors identified two instances where the licensee determined, based on

a review of information provided by vendors, that design margins or instructions

in safety-related calculations or procedures were adversely impacted but failed to

revise the calculations or procedures to reflect these non-conservative

assumptions.

Description. On April 9, 2009, the licensee initiated Nuclear

Notification 200385686 to evaluate Westinghouse Technical Bulletin TB-09-4.

This technical bulletin identified that auxiliary feedwater pump heat was not

explicitly considered in the sizing calculation for the condensate storage tank;

addition of this heat could have an effect of approximately 3000 gallons on the

required condensate storage tank volume. On September 25, 2009, the licensee

completed its evaluation of this technical bulletin. The licensee concluded that

\Nhi!e Technical Bulletin T8-09-4 'vvas applicable to San Onofre Nuciear

Generator Station, there was sufficient margin in the existing calculation for the

system to perform according to design requirements; no further action was

- 46- Enclosure 2

necessary. The affected calculation was not updated. The inspectors verified

the licensee's determination that the non-conservatism addressed in the

technical bulletin was bounded by other assumptions in the condensate storage

tank sizing calculation. However, the inspectors determined that the failure of the

licensee to note the neo-conservatism in the calculation could result in the loss of

margin should the bounding assumptions be changed in the future. The licensee

initiated Nuclear Notification 200886265 to address this deficiency.

On November 5, 2009, the licensee initiated Nuclear Notification 200656309 to

evaluate Westinghouse Nuclear Safety Advisory Letter NSAL-09-8. This letter

identified the potential for the presence of vapor in emergency core cooling and

residual heat removal systems during certain modes of operation. The letter

identified the potential that if the residual heat removal system is operated in the

shutdown cooling mode above 200°F, initiation of safety injection following a loss

of coolant accident could result in the injection water flashing to steam, binding

the low pressure safety injection pumps. On January 14, 2010, the licensee

completed its evaluation of this nuclear safety advisory letter and determined that

while it was appiicabie to San Onofre Nuclear Generator Station, the concerns

noted in the letter had already been addressed in San Onofre Nuclear Generator

Station procedures or instructions which contained cautions against operation of

shutdown cooling above 200°F. A task was generated under Nuclear

Notification 200656309 to modify San Onofre Procedure S023-5-1.3, "Plant

Startup from Cold Shutdown to Hot Standby," Revision 35, to note flashing of

injection water as a reason shutdown cooling operation should be secured in

Mode 5 prior to entering Mode 4. This task was improperly characterized as an

plant modifications or modification-related, procedure and assigned a due date of

June 30, 2010. During a review of all plant modification procedure change

requests requested by the inspectors, the licensee determined that the plant

modification classification was inappropriate and changed it to an "E," or

enhancement. The inspectors determined that this procedure change should

have properly been classified as a "T," or technical change, and been

implemented prior to the next use of the procedure during reactor startup.

On March 26, 2010, during reactor startup following Unit 2 outage R2C16, the

licensee was operating in Mode 4 at approximately 270°F while attempting to

restore one train of auxiliary feedwater. When this restoration was delayed, the

licensee's risk analysis group advised the operators to place shutdown cooling in

standby to provide an alternate source of core cooling should the single operable

train of auxiliary feedwater be lost. Because the procedure only noted that

reactor coolant temperature "should" be maintained below 200°F while shutdown

cooling is in operation and did not reference the conclusions drawn from the

licensee's analysis of NSAL-09-8, operations personnel failed to recognize the

vulnerability of the system to flashing and vapor binding the pump on initiation of

low pressure safety injection. Referencing a note contained in the limitations

section of the procedure (Attachment 12, Step 15.1) which states, "When

shutdm,Am cooling is in-service, then [ieactor coolant system] temperature ... shaH

not exceed 340°F ... ," operations personnel began taking steps to place

shutdown cooling in standby with reactor coolant temperature at approximately

- 47- Enclosure 2

270°F. After this course of action was questioned by the NRC resident

inspectors and station management, the licensee identified the operating

experience evaluation performed under Nuclear Notification 200656309 and

determined that placing shutdown cooling in standby at 270°F was inappropriate

with current procedures. The licensee initiated Nuclear Notification 200855352

to identify why this course of action was considered.

The licensee's review of NSAL-09-8 under Nuclear Notification 200656309 also

identified that while cooling down, San Onofre Procedure S023-3-2.6, "Shutdown

Cooling System Operation," Revision 26, contains procedural steps to isolate the

suctions of the low pressure safety injection pumps prior to the initiation of

shutdown cooling. However, the inspectors noted that, similar to the startup

situation, there is no procedural step or limitation to indicate that these valves

must be shut above 200°F to prevent flashing of the fluid should a safety injection

signal be received. Further, the limitations and specifications section of the

procedure (Attachment 16, Step 1.1) only restricts operation to at or below

340°F. In its evaluation of NSAL-09-8, the licensee did not initiate a procedure

change request to address this vulnerability in this procedure. Because

procedural restrictions in both San Onofre Procedures S023-5-1.3 and

S023-3-2.6 permit shutdown cooling operation up to 340°F and because

Section 5.4.7 of the Final Safety Analysis Report specifies that shutdown cooling

is put into service once reactor coolant system temperature has been reduced

below 350°F, the inspectors determined that site procedures and design basis

documentation are inadequate to ensure that operators do not place shutdown

cooling in service above 200°F.

Analysis. The failure of the licensee to maintain plant design basis

specifications, drawings, procedures, and instructions up-to-date is a

performance deficiency. The finding is of more than minor significance because

it adversely affects the design control attribute of the Mitigating Systems

Cornerstone objective. Using Inspection Manual Chapter 0609.04, Phase 1,

"Initial Screening and Characterization of Findings," the finding was determined

to have a very low safety significance because the finding did not result in a loss

of system safety function, an actual loss of safety function of a single train for

greater than its technical specification allowed outage time, or screen as

potentially risk significant due to a seismic, flooding, or severe weather initiating

event. The finding has a crosscutting aspect in the area of problem identification

and resolution associated with the operating experience component because the

licensee failed to implement and institutionalize operating experience information,

including vendor recommendations, through changes to plant processes,

procedures, equipment, and training programs. P.2(b)

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion III, "Design Control,"

requires, in part, that measures be established to assure that the design basis for

safety-related structures, systems, and components are correctly translated into

specifications, dravvings, procedureS, and instructions. Contrary to tJlis

requirement, on June 27,2009, September 25,2009, and January 14, 2010, the

licensee failed to assure that the design basis for safety-related structures,

- 48- Enclosure 2

systems, and components was correctly translated into specifications, drawings,

procedures, and instructions. Specifically, the licensee identified

nonconservative errors in calculations and procedures but failed to incorporate

this new information into the affected calculations and procedures. Because this

finding was of very low safety significance, was not repetitive or willful, and was

entered into the corrective action program, this violation is being treated as a

noncited violation, consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000361 ;05000362/2010006-12, "Failure to Maintain Design Basis

Information."

m. Failure to Meet Action Plan for Substantive Crosscutting Issues

Introduction. The inspectors identified a Green finding involving examples of the

licensee's failure to meet its action plan as described in letters to the NRC

documenting actions San Onofre Nuclear Generator Station would take to correct

the third and fourth consecutive assessment cycles of substantive crosscutting

issues in the areas of human performance and problem identification and

resolution.

Description. The NRC's annual assessment letter dated March 4,2009, was the

third cycle where substantive crosscutting issues were identified in human

performance and problem identification and resolution. San Onofre Nuclear

Generator Station responded to the open substantive crosscutting issues in a

letter titled, "Response to Annual Assessment Letter Inspection

Report 05000361/2009001, 05000362/2009001," dated April 21,2009, with the

status of corrective actions planned to address the human performance and

problem identification and resolution crosscutting issues, including schedules,

milestones, and performance monitoring metrics. San Onofre Nuclear Generator

Station committed to completing six initiatives to improve its human performance

and eight initiatives to improve its process for problem identification and

resolution. The licensee committed to completing specific actions to improve

performance in these areas.

The status of these commitments was provided to the NRC in an

October 30, 2009, letter. As of that date:

  • Of the 48 commitments made to improve performance in the human

performance area, 28 were complete. Of the 20 remaining open, 4

(20 percent) were past due.

  • Of the 36 commitments made to improve performance in the problem

identification and resolution area, 21 were complete. Of the 15 remaining

open, 3 (20 percent) were past due.

Several of the specific actions to which the licensee committed were not

compieted by theii specified due dates and/or were not compieted as specified,

as evidenced by the following examples:

- 49- Enclosure 2

i. The licensee committed to establishing response inspectors training and

providing this training to selected personnel by December 31,2009. As

of March 31,2010, this training had not been completed.

ii. The licensee committed that divisions that were not meeting apparent

cause evaluation timeliness goals would develop action plans to improve

apparent cause evaluation timeliness to less than or equal to 40 days by

December 10, 2009. As of March 31, 2010, these divisions had not

developed action plans. In a letter dated March 31, 2010, the licensee

revised the language of this commitment to reflect actions taken.

iii. The licensee committed to establishing a specific work down curve and/or

schedule for backlog of actions requiring closure review boards by

February 20, 2010, so that by March 2010, closure review boards were

normally completed within 30 days of action completion. As of

March 31,2010, the licensee had failed to establish work down curves or

schedules and closure review boards were not being completed in a

timely fashion.

On October 29, 2009, after completing an independent safety culture survey in

which it noted several areas requiring improvement, the licensee sent another

letter to the NRC committing to 56 specific actions to resolve these issues. Five

areas requiring action to preserve and improve safety culture were identified.

The licensee committed to completing specific actions in each of these areas by

specified due dates. Several of the specific actions to which the licensee

committed were not completed by their specified due dates and/or were not

completed as specified, as evidenced by the following examples:

i. The licensee committed to establishing a specific work down curve andlor

schedule for backlog of actions requiring closure review boards and

implement by February 20, 2010, so that by March 2010, closure review

boards were normally completed within 30 days of action completion. As

of March 31, 2010, the licensee had failed to establish work down curves

or schedules and closure review boards were not being completed in a

timely fashion.

ii. The licensee committed to establishing a project plan and schedule for

resolving SAP issues by February 15, 2010, that included: mechanisms

for employee input on problems and solutions; definition of end-state

desired performance; implementation of improvements; and evaluation of

effectiveness. As of March 31, 2010, the licensee had failed to establish

a project plan as specified.

On March 25, 2010, the licensee initiated Nuclear Notification 200848923, noting

that "a number of the commitments to the NRC iTrade in the October 29, 2009,

and October 30, 2009, letters ... were completed with inadequate initial quality or

were completed late." On March 31,2010, the licensee submitted a letter to the

- 50- Enclosure 2

NRC modifying some of these commitments. Specifically, the licensee changed

the wording for 19 committed actions to reflect the actions taken, which did not

align with the actions initially committed, including due date changes for nine

past-due commitments for which the licensee changed the due date to a future

date. As a result, the licensee failed to satisfy several commitments and due

dates made to the NRC related to corrective actions to correct the substantive

crosscutting areas. In addition, the licensee modified commitments without first

discussing the changes with the Nuclear Regulatory Commission.

Also, the licensee's letters dated April 21, 2009, identified the metrics by which

the licensee would assess the state of its corrective action program. The

inspectors reviewed the metrics and identified several questions regarding the

data the licensee was evaluating for its metrics. Examples included: 1

  • The metric for measuring the time to perform root cause evaluations has

been relatively flat over the monitoring period; the metric for measuring

the time to perform apparent cause evaluations has exhibited a

downward (improving) trend. However, the inspectors found that these

metrics are tracked from the assignment date to the "Evaluation Complete

Date." As discussed in Nuclear Notification 200886035, the assignment

date can be weeks or months after the issue/event was discovered before

San Onofre Nuclear Generator Station begins counting time against the

metric; and San Onofre Nuclear Generator Station stops counting time

against the metric after the divisional corrective action program

coordinator review which can be weeks or months before final approval

by the corrective action review board. Thus, the data for the time to

perform cause evaluations does not reflect the true time it takes the

licensee to assign and complete the cause evaluation until the time the

corrective actions are identified and approved.

For example:

o At the corrective action review board on April 19, 2010, an

apparent cause evaluation charter was approved for a notification

that was originally written on December 19, 2009. As of

April 20, 2010, the apparent cause evaluation had not been

assigned; therefore, the clock had not started to track the metric.

Thus, the metric for this evaluation did not account for about four

months of time.

o At the corrective action review board on April 19, 2010, an

apparent cause evaluation was approved that had been started on

November 15, 2009, for a notification generated on

November 13, 2009. San Onofre Nuclear Generator Station

stopped counting time for purposes of the metric when the

I Unless otherwise mentioned, all examples cover metrics tracked from July 2009 through February 20 I o.

- 51 - Enclosure 2

divisional corrective action program coordinator approved the

corrective action on January 22, 2010; yet final approval did not

actually occur until the corrective action review board on

April 19, 2010. Thus, the metric for this evaluation did not account

for about three months of time.

.. Licensee management had explained to NRC inspectors that their

upward trend in the number of nuclear notifications written demonstrates

an improvement in the corrective action program in that more people are

using it. However, this data only goes back through July 2009. While

there was a marked increase in the number of nuclear notifications

generated over the first few months of the period, the number has since

been constant. 2 The overall increase in nuclear notifications did not

account for the expected increase in nuclear notifications from a larger

number of personnel on site and the larger workload during the recent

extended outage.

  • Similarly, licensee management has cited the declining average age of

open actions as an indicatOi of improvement. However, while the

average age of corrective actions related to cause evaluation has been

trending steadily downward, this appears to be largely due to a concerted

effort by the licensee to work off the oldest corrective actions rather than

a true overall reduction in the age of corrective actions. Further, this

metric does not track the average age of corrective actions to prevent

recurrence, which has been trending sharply upward.

.. The number of nuclear notifications open has demonstrated a significant

upward trend since November 2009. In its April 21, 2009, letter to the

NRC, the licensee committed to reducing the number of open nuclear

notifications, in part by developing actions to reduce backlog for each

division not meeting its divisional metric. On April 14, 2010, the closure

review board package related to this commitment was closed, with the

statement that the metric had been met for 2009. However, this

commitment was modified by the licensee's March 31, 2010, letter which

stated that the 2009 goals had been met; that the licensee was now

focusing on 2010 goals. The commitment was closed as having been

accomplished; however, this metric has been red and trending upward

since January 2010.

Analysis. The inspectors determined that the licensee's failure to perform actions

as documented in its plan to the NRC was more than minor because if left

uncorrected could result in a more significant safety concern. Using Inspection

Manual Chapter 0609, Appendix M, this finding was reviewed by NRC

management and was determined to be of very low safety significance (Green).

2 Significance level 5 and lower exhibit a slight upward trend over the past three months; significance level 1-4

nuclear notification generation has been trending slightly downward over the same period.

- 52 - Enclosure 2

The finding has a crosscutting aspect in the area of human performance

associated with the work practices because the licensee did not ensure

management oversight of work activities. H.4(c)

Enforcement. The finding does not involve an enforcement action because no

violation of regulatory requirements was identified. Because the finding does not

involve a violation and it has very low safety significance, it is identified as

FIN 05000361 ;05000362/201 0006-13, "Failure to meet action plan for

substantive crosscutting issues."

40A6 Meetings

Exit Meeting Summary

On April 23,2010, the inspectors conducted a briefing of the status of potential findings before

concluding the onsite portion of the inspection. This briefing was presented to

Mr. R. Ridenoure, Senior Vice President and Chief Nuclear Officer, and other members of the

licensee staff. At the conclusion of the inspection on June 17, 2010, the inspectors conducted

an exit briefing with Mr. Ridenoure and other members of the licensee staff. The licensee

acknowledged the issues presented. The inspectors asked the licensee whether any materials

examined during the inspection should be considered proprietary. No proprietary information

was identified.

40A6 licensee-Identified Violations

The following violations of very low safety significance (Green) were identified by the licensee

and are violations of NRC requirements which meet the criteria of Section VI of the NRC

Enforcement Policy, or being dispositioned as NCVs.

Green. The inspectors reviewed a licensee-identified finding involving the failure to follow San

Onofre Procedure S0123-1-1.3, "Work Activity Guidelines," Revision 26, Step 6.18.2.2, which

allows the licensee to skip a preventive maintenance work order step as long as an evaluation is

documented that identifies why it is okay not to perform the step. Specifically, in March 2006,

the licensee identified that cubicle for breaker 2A0807 had not been cleaned prior to Cycle 7

due to an energized reserve auxiliary transformer and generated Action Request 060300521 to

document the deficiency. The action request further indicated that this issue was applicable to

all of San Onofre Nuclear Generator Station 4.16 kV switchgear. All of the switchgears (A03,

A04, A05, A06, A07, A08, and A09 for both units) have feeders from both the reserve auxiliary

and unit auxiliary transformers (the GDC 17 off-site source of power). The licensee stated that it

was not possible to clean every cubicle in a given bus within a single work window. The

manufacturer recommended a cleaning frequency of five years of 1000 cycles of operation;

however, cubicle for breaker 2A0807 had not been cleaned in over 14 years without an

evaluation documenting a basis for postponing the preventive maintenance. Licensee

personnel entered this issue into their corrective action program as Nuclear

Notifications 200876216 and 200880374.

This finding was more than minor because it impacted the human performance attribute of the

Initiating Events Cornerstone objective to limit the likelihood of those events that upset plant

- 53- Enclosure 2

stability and challenge critical safety functions during shutdown as well as power operations.

Using Inspection Manual Chapter 0609.04, Phase 1, "Initial Screening and Characterization of

Findings," the inspectors determined the finding to be of very low safety significance (Green)

because it did not contribute to both the likelihood of a reactor trip and the likelihood that

mitigation equipment or functions would not be available. This finding was determined not to

have a crosscutting aspect because it is a latent condition.

- 54- Enclosure 2

KEY POINTS OF CONTACT

Licensee Personnel

C. Amundson, Maintenance Engineer

V. Barone, Design Engineer

R. Battish, System Engineer

G. Becker, Operations Procedures

S. Chun, Maintenance Engineering Manager

S. Gardner, Electrical Supervisor, System Engineering

J. Jay, Site Procedures Manager

J. Madigan, Health Physics Manager

A. Martinez, Corrective Action Program Manager

A. Matheny, System Engineer

M. McBrearty, Licensing Engineer

C. Mitchell, Operations Procedures

J. Osborne, Project Manager

T. Remick, Engineer, Nuclear Fuel Management

R. Sandstrom, Manager, CAP Project

A. Shean, Nuclear Oversight Manager

NRC personnel

R. Caniano, Director, Division of Reactor Safety

M. Hay, Chief, Technical Support Branch

M. Shannon, Chief, Plant Support Branch 1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000361/2010006-01 NCV Inadequate Operability Determination for Turbine-Driven

Auxiliary Feedwater Pump Steam Admission Valves

(Section 40A2.5a)05000361/2010006-02 NCV Failure to Translate Design Basis Information for Turbine-

Driven Auxiliary Feedwater Pump Steam Admission

Valves (Section 40A2.5b)05000361/2010006-03 NCV Lack of Preventive Maintenance Results in Valve Failure

and Inoperable Condensate Storage Tank

(Section 40A2.5c)05000362/2010006-04 NCV Failure to Report Conditions That Could of Prevented

Fulfillment of Safety Function (Section 40A2.5d)

A-1 Attachment

Opened and Closed

05000362/2010006-05 NCV Control Room Operators' Failure to Adhere to Conduct of

Operations Procedural Requirements (Section 40A2.5e)05000361/2010006-06 NCV Failure to Provide Adequate Procedure for Boron Dilution

Activities (Section 40A2.5f)05000361/2010006-07 NCV Failure to Establish Component Cooling Water Radiation

ivionitoring Procedures (Section 40A2.5g)05000361/2010006-08 NOV Failure to Maintain Written Procedures Covered In

05000362/2010006-08 Regulatory Guide 1.33 (Section 40A2.5h)05000361/2010006-09 NCV Failure to Establish Goals And Monitor for A(A) Auxiliary

05000362/2010006-09 FeedlJJater Trains (Section 40A2.5i)05000361/2010006-10 NCV Failure to Identify and Correct Use of Deficient

05000362/2010006-10 Relays (Section 40A2.5j )05000361/2010006-11 NCV Failure to Secure Loose Items in the Electrical Switchyard

05000362/2010006-11 (Section 40A2.5k)05000361/2010006-12 NCV Failure to Maintain Design Basis Information

05000362/2010006-12 (Section 40A2.5!)05000361/2010006-13 FIN Failure to Meet Action Plan for Substantive Crosscutting

05000362/2010006-13 Issues (Section 40A2.5m)

Discussed

None

LIST OF DOCUMENTS REVIEWED

NUCLEAR NOTIFICATIONS

051001450 200000500 200002210 200002831 200003235

200005532 200005669 200006247 200006366 200006369

200006446 200038227 200047962 200047966 200051692

200052533 200057409 200057494 200057495 200059017

200059581 200060319 200062659 200063244 200080798

200081823 200085457 200095432 200096864 200105838

200112302 200114904 200145364 200146292 200149442

200161642 200166828 200173442 200177549 200177574

200179975 200182897 200184754 200184925 200185228

200187140 200187174 200187386 200188818 200188819

200188863 200189008 200191575 200191643 200191644

A-2 Attachment

NUCLEAR NOTIFICATIONS

200191645 200193463 200194565 200196248 200198876

200199177 200199779 200199803 200200494 200200611

200202392 200202393 200204501 200207687 200209764

200210468 200214923 200216417 200216513 200216785

200217658 200220855 200220901 200224995 200226676

200226851 200229880 200231408 200232002 200237510

200240476 200243930 200244824 200244829 200245222

200249395 200253140 200253911 200253923 200256206

200256262 200258836 200262707 200273137 200281150

200283647 200289984 200301597 200304171 200305694

200309516 200310250 200318226 200319240 200321468

200323460 200323662 200327156 200329766 200337121

200339686 200346192 200347912 200348622 200348676

200350707 200351309 200353559 200353830 200354725

200356209 200357930 200358255 200360012 200362207

200362248 200366460 200375226 200375263 200375271

200375476 200378003 200378783 200383586 200383717

200385686 200385833 200388215 200388299 200389219

200389465 200389602 200391307 200396072 200396074

200396078 200396106 200397538 200402044 200402733

200403327 200403903 200403904 200403907 200403931

200403942 200404016 200407083 200407263 200407581

200408677 200408745 200411720 200413389 200413417

200414063 200414385 200416902 200417206 200420952

200423048 200424908 200425771 200427466 200427700

200439005 200442871 200445728 200449046 200450694

200453351 200454549 200454708 200454875 200456738

200457151 200458808 200461737 200462842 200463613

200469510 200476904 200481911 200493704 200495283

200496192 200498067 200498776 200501125 200505402

200507991 200509834 200511477 200514597 200518579

200545007 200545500 200550606 200550985 200553431

200554449 200554503 200554762 200556120 200559128

200564587 200569111 200572704 200581670 200585309

200591743 200596242 200596804 200599691 200599743

200600926 200604461 200607694 200611851 200613666

200613716 200614081 200625389 200628825 200631222

200631367 200635119 200636471 200636549 200638562

200638824 200640096 200647126 200656309 200657895

200663614 200663620 200663692 200664434 200666345

200666345 200666778 200667666 200668488 200670338

200683591 200684138 200685073 200688490 200688648

200689102 200689282 200689526 200689551 200689650

"'U("".""\.",,,...,...

')()()aC()A()O

&-vvv.;../v-rvu

....,f'\n~f'\no-,n-

&:.VVV;::JVOIO

1""\ 1"\

.c.UUO::1U::1UU 20069097-i 200691209

200691226 200691370 200691516 200692319 200692334

200692335 200692347 200692815 200692819 200694409

A-3 Attachment

NUCLEAR NOTIFICATIONS

200698869 200699499 200703718 200703793 200704636

200704875 200710313 200711245 200711324 200711339

200711991 200712412 200715724 200718801 200721702

200722117 200727789 200728270 200728441 200737719

200743785 200743785 200745033 200746950 200752137

200760309 200761459 200769308 200778595 200778598

200780929 200781022 200791845 200792682 200801929

200803364 200804931 200805827 200809842 200814132

200832315 200834923 200835619 200836042 200841643

200847163 200848923 200853352 200858260 200866485

200866488 200866490 200867104 200870138 200871526

200871527 200874078 200876130 200876216 200877698

200877796 200877799 200877834 200880374 200882433

200886035 200887746 200887995 200888919

ORDERS

800011270 800049251 800073513 800073728 800076896

800076907 800081649 800164561 800183273 800185541

800192268 800216674 800216676 800216677 800216678

800269843 800275473 800289258 800314547 800354225

CONDITION REPORTS/OTHER

AR 020201440 AR 020201440 AR 020201440 AR 020801305 AR 020801305

AR 020801305 AR 020801305 AR 030100348 AR 030100348 AR 030100348

AR 030100348 AR 030401460 AR 030401460 AR 030401460 AR 041200133

AR 041200133 AR 041200133 AR 050401537 AR 050401537 AR 050401537

AR 060300521 AR 060300521 AR 060300521 AR 060301666 AR 060301666

AR 060301666 AR 061200817 AR 061200817 AR 061200817 AR 070500851

AR 070500851 AR 070500851 AR 070700345 AR 070700345 AR 070700345

AR 070700366 AR 070700366 AR 070700366 AR 070800283 AR 070800283

AR 070800283 AR 070800284 AR 070800284 AR 070800284 AR 070800285

AR 070800285 AR 070800285 AR 070800286 AR 070800286 AR 070800286

AR 070800287 AR 070800287 AR 070800287 AR 070800288 AR 070800288

AR 070800288 AR 070800289 AR 070800289 AR 070800289 AR 070800993

AR 070800993 AR 070800993 AR 071000901 AR 071000901 AR 071000901

AR 071200416 AR 071200416 AR 071200416 AR 071201393 AR 071201393

AR 071201393 AR 071201417 AR 071201417 AR 071201417 AR 080101417

AR 080101417 AR 080101417 AR 080200546 AR 080200546 AR 080200546

AR 080300666 AR 080300666 AR 080300666 AR 080301122 AR 080301122

AR 080301122 AR 080301404 AR 080301404 AR 080301404 AR 080400545

AR 080400545 AR 080400545 AR 080401137 AR 080401137 AR 080401137

AR 080401137 AR 080401144 AR 080401144 AR

  1. ....

()~()L!()11AA

..... _v lV f I,-r

I\DI"IOI"IAI"I-1-1AA

I\I'\. uuv*"tV I f"t

AR 080500972 AR 080500972 AR 080500972 AR 080600104 AR 080600104

AR 080600104 AR 080600212 AR 080600212 AR 080600212 RCE 93-004

A-4 Attachment

ENGINEERING DOCUMENTS

NECP 800071431 NECP 800071494 NECP 800071495 NECP 800071764

NECP 800071869 NECP 800074314 NECP 800074316 NECP 800074486

NECP 800129634

MAINTENANCE ORDER

06101428 0412153600 05101896000

PROCEDURES

NUMBER REVISION / DATE

Replacement of Foxboro CVCS Boric Acid Makeup 0

System Controls with Ovation Distributed Control

System (DCS)

Shutdown Nuclear Safety 24

2-10-010 Operating Instruction Attachment 7 Boron Saturating January 26, 2010

2(3)ME-074, CVCS Ion Exchanger

A610 Operation of Manual (Gearbox) Butterfly Valves 21

Attachment 29

LCS 3.3.108 Vibration and Loose-Parts Monitoring System

M-0050-017 BTB RSB 5-1 Condensate Inventory Calculation 4

N/A SONGS System Health Report, 4KVS 4th Quarter, 2009

SCES-004-08 Corrective Action Program Audit May 16, 2008

SCES-012-09 Equipment Reliability Audit October 17, 2009

SCES-014-09 Corrective Action and Self-Assessment Program March 5, 2010

Audit

SD-S023-110 220 kV Switch yard System 19

SD-S023-120 6.9 kV, 4.16 kV, and 480 V Electrical Distribution 19

Systems

S0123-0-A6 Operations Division Procedure (Precautions) 8

S0123-!-1.28.1 Electric Distribution Grounding Guide

A-5 Attachment

PROCEDURES

NUMBER REVISION I DATE

S0123-0-A6 Operations Division Procedure (Precautions) 8

S0123-1-1.28.1 Electric Distribution Grounding Guide 4

S0123-1-1.3 Work Activity Guidelines 26

S0123-1-1.3 Work Activity Guidelines 26

S0123-1-1.34 Scaffolding Erection 27

S0123-1-4.13 Megger Testing 6

S0123-1-9.9 Square "0" and Westinghouse Type OS Circuit 4

Breakers Inspection and Testing

SO 123-11-9.48 Magnetrol and Other Miscellaneous Liquid Level 6

Switches Calibration

S0123-MA-1 Maintenance and Construction Services Division 7

S0123-MA-1 Maintenance and Construction Services Division 7

S0123-0R-1 Operating Experience Program 9

S0123-RX-1 Reactivity Management Program 4

S0123-VI-1 Review/Approval Process for Orders, Procedures, 28

and Instructions

S0123-XV-1.20 Seismic Controls o

S0123-XV-109 Procedure and Instruction Format and Content 1

S0123-XV-109.1 Procedure Action Request Committee (PARC)

Process

S0123-XV-3.3 NRC Reporting Requirements and Assessments 15 EC 15-1

S0123-XV-303 Closure Review Process o

S0123-XV-50 Corrective Action Program 15

S0123-XV-50 Corrective Action Program 16

Functionality Assessments and Operabiiity 14

Determinations

A-6 Attachment

PROCEDURES

NUMBER TITLE REVISION I DATE

S0123-XV-91 Reactivity Management Implementation 4

SO 123-XV-H U-1 Human Performance Program 6

S0123-XV-HU-4 Human Performance Roles and Responsibilities 1

S0123-XX-11 Switchyard Work Performance 2

S0123-XX-11 Switch yard Work Performance 2

S0123-XX-6 Operator Work Around Program 7

S0123-XXIV-5.1 Engineering & Technical Services Software Quality 6

Assurance

S0123-XXX-3.5 Evaluation and Reporting of Problems to the NRC 3

Pursuant to 10 CFR Part 21

S0123-XXX-3.5 Evaluation and Reporting of Problems to the NRC 3

Pursuant to 10 CFR Part 21

S0123-XXXVI-1 Nuclear Fuel Management (NFM) Quality Program 6

S023-10-9 Turbine Lube Oil System Operation 19

S023-13-8 Severe Weather 8

S023-13-8 Severe Weather 8

S023-15-53.A CIRC Water Box Cathodic Protection Sys Trouble 20

S023-15-53B Condensate Pump P050 Flow Lo 18

S023-15-63.o Annunciator Panel 63D, Switchyard/Penetration 12

Switchgear

S023-15-63.E Annunciator Panel 63E, Switchyard 8

S023-3-2.4 Operating Instruction Attachment 7 Boron Saturating 21

2(3)ME-074, CVCS Ion Exchanger

S023-3-2.4 Operating Instruction Attachment 7 Boron Saturating 22

2(3)ME-074, CVCS Ion Exchanger

S023-3-2.6 Shutdown Cooling System Operation 26

A-7 Attachment

PROCEDURES

NUMBER TITLE REVISION I DATE

S023-3-3.30A Main Steam System Online Valve Test 12

S023-3-3.S Safety Injection Monthly Tests 25

S023-5-1.3 Plant Startup from Cold Shutdown to Hot Standby 35

S023-6-25 Generator Stator Cooling Water System Operation 23

S023-6-30 230kV Switch yard Rounds and Inspections 26

S023-6-30 Switch yard Inspection and Operation 26

S023-6-30 Switchyard Inspection and Operation 27

Main and Auxiliary Transformer Operation 20

S023-6-6 Reserve Auxiliary Transformer Operation 15

S023-IV-6.3.2 Security Intrusion Detection System Probability 7

Testing

S023-V-16 Emergency Core Cooling System (ECCS) Piping Gas 0

Void Calculation

S023-V-2.14 Thermal Inspection of Plant Components 9

S023-V-2.14 Thermal Inspection of Plant Components 9

S023-V-4AO Electrical Equipment Monitoring Program 4

S023-V-4.40 Electrical Equipment Monitoring Program 3 TCN 3-1

S023-V-4AO Electrical Equipment Monitoring Program 3

S023-XV-2 Troubleshooting Plant Equipment and Systems 6

S023-XV-50.CAP-1 Writing Nuclear Notification for Problem Identification 3

and Resolution

S023-XV-50.CAP-2 SONGS Nuclear Notification Screening 5

S023-XV-50.CAP-4 Implementing Corrective Actions 3

S023-XV-S5 Boric Acid Corrosion Control Program (BACCP) Top 5

Risk Significant Systems

A-S Attachment

PROCEDURES

NUMBER TITLE REVISION I DATE

S023-XX-10 Maintenance Rule Risk Management Program 3

S023-XX-10 Maintenance Rule Risk Management Program 3

Implementation

On-Line itVork Management Process 3

S023-XX-29.1 Seasonal Readiness 0

S023-XX-30 Nuclear Maintenance Order (NMO) Generation, 1

Screening, and Classification

S023-XX-30 Nuclear Maintenance Order (NMO) Generation, 2

Screening and Classification

S023-XX-8 Integrated Risk Management 5

S023-XXXVI-1.4 Documentation of Reload Fuel Cycle Analysis 6

SOS-025-09 Surveillance Report: Corrective Action Program May 26, 2009

Implementation

SOS-040-09 Surveillance Report: Station Integrated Business October 09, 2009

Plan Closure Review Process

SY -S023-G-2 Systems Engineering Handbook 4

SY-S023-G-2 Systems Engineering Handbook 3

SY-S023-G-2 Walkdown Standard-Stainless Steel Schedule 10S 4

Pipe

TM-2791A SONGS Air Management From RWST and CES July 2008

Licensee Meetings Attended

Production/Ops Focus Meeting (2)

Closure Review Board (CRB) (3)

Corrective Action Review Board (CARB) (2)

SONGS Switchyard Oversight Committee (SSOC) (1)

A-9 Attachment

OTHER MISCELLANEOUS DOCUMENTS

TITLE

Leadership Engagement Trending System Engagement Summary November 2009 to

Report March 2010

Unit 2/3 Operations Leadership Observation RAA-Plant Monitor 1st Quarter, 2010

Reactivity Affecting Activiiy LOP 14

Fundamental LOP 14 RAA-Plant Monitor Reactivity Affecting Activity April 6, 2010

From 10/01/2009-10/31/2009

Monthly Meeting Reactivity Oversight Group (ROG) March 30, 2010

ROG Report-Meeting 03/30/2010 March 30, 2010

List of Operator Workarounds July 2009 to

November 2009

List of Operator Burdens December 2009 to

January 2010

List of Control Room Issues July 2009 to

January 2010

List of Temp Mods October 2009 to

March 2010

List of Control Room Deficiencies April 2009 to

February 2010

SONGS Operational Focus Index April 6, 2010

Operations Division Corrective Action Burndown Plan November 6,2009

Leadership Engagement Trending System 10.14 RAA-PLANT Monitor February 2010

Reactivity Affecting Activity (LOP 14)

Impaired Alarm Record Unit 2

Priority 1 HPSI Pump Control Circuits (Implementation of ECP that June 5, 2009

corrects problem)

Top Ten Equipment Issues at SONGS

Leadership Engagement Trending System 10.19 Verification Practices

(LOP 19)

A-10 Attachment

OTHER MISCELLANEOUS DOCUMENTS

TITLE

Site Plan Status Control Misposition Events

Mission Times for Operability Determinations Rev A

February 24, 2010

March 2010

Gas Void Trend in 8" LPSI Header (U2 Loop 2A) March 2009 to

September 2009

Root Cause Directed Maintenance Evaluation dated September 1995 "RCDM 95-02 "Design

Life of Normally Energized Agastat E700017000 Series Time Delay Relays" lAW NA TS No.

9509010". (This study found that the relays have a design life much longer than the 10 years

specified by the manufacturer and that the actual design life was greater than 40 years)

CALCULATIONS

NUMBER SUBJECT

M-0013-005 Safety Injection Tank Fluid Nitrogen Evolution

ACTION REQUESTS

050100895 050101779 050200370 050200417 050201676

050300921 050600035 050600474 050800143 050800896

051101380 051200838 051200895 060100358 060100673

060101480 060101481 060200732 060300521 060401277

060501595 060600040 060700177 060700430 060701103

060701128 060800908 060800909 060800962 060900185

060900824 060900981 061000969 061001517 061001528

061100693 061101379 061101448 061101460 061101464

061101478 061101632 070300300 070300991 070301057

070500395 070500760 070801108 071100540 071100697

071101406 071101426 071101427 071101428 071101429

071101431 071101432 071200061 071200215 071200331

071200546 071200614 071200621 071200927 071201038

071201039 071201169 071201203 071201205 071201245

071201468 071201558 071201814 080100008 080100688

080100844 080200815 080200903 080201125 080300231

080300994 080400273 080400955 080500248 080500381

080501351 080600108 080600397

A-11 Attachment

DRAW INGS

NUMBER TITLE REVISION

30342 Elementary Diagram Diesel Generator 2G002 Control DC System

11

30344 Elementary Diagram Diesel Generator 2G002 Excitation

14

A-12 Attachment