ML100420026

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IR 05000361-09-005, 05000362-09-005; on 09/24/2009 - 12/31/2009; San Onofre Nuclear Generating Station, Units 2 & 3, Integrated Resident an Regional Report; Flood Prot. Meas., Maint. Effect., Operability Evaluations, Event Follow-up, & Othe
ML100420026
Person / Time
Site: San Onofre  Southern California Edison icon.png
Issue date: 02/11/2010
From: Ryan Lantz
NRC/RGN-IV/DRP/RPB-D
To: Ridenoure R
Southern California Edison Co
References
FOIA/PA-2011-0221, FOIA/PA-2011-0157 IR-09-005
Download: ML100420026 (97)


See also: IR 05000361/2009005

Text

UNITED STATES

NUC LE AR RE G UL AT O RY C O M M I S S I O N

R E GI ON I V

612 EAST LAMAR BLVD , SU I TE 400

AR LI N GTON , TEXAS 76011-4125

February 11, 2010

Mr. Ross T. Ridenoure

Senior Vice President and

Chief Nuclear Officer

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

SUBJECT: SAN ONOFRE NUCLEAR GENERATING STATION - NRC INTEGRATED

INSPECTION REPORT 05000361/2009005 and 05000362/2009005

Dear Mr. Ridenoure:

On December 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your San Onofre Nuclear Generating Station, Units 2 and 3 facilities. The

enclosed integrated inspection report documents the inspection findings, which were discussed

on January 13, 2010, with you, and other members of your staff.

The inspections examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report documents nine NRC identified findings and one self-revealing finding of very low

safety significance (Green). Eight of these findings were determined to involve violations of

NRC requirements. Additionally, three licensee-identified violations, which were determined to

be of very low safety significance, are listed in this report. However, because of the very low

safety significance and because they are entered into your corrective action program, the NRC

is treating these findings as noncited violations, consistent with Section VI.A.1 of the NRC

Enforcement Policy. If you contest the violations or the significance of the noncited violations,

you should provide a response within 30 days of the date of this inspection report, with the basis

for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, D.C. 20555-0001, with copies to the Regional Administrator, U.S. Nuclear

Regulatory Commission, Region IV, 612 E. Lamar Blvd, Suite 400, Arlington, Texas,

76011-4125; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission,

Washington, D.C. 20555-0001; and the NRC Resident Inspector at the San Onofre Nuclear

Generating Station facility. In addition, if you disagree with the characterization of any finding in

this report, you should provide a response within 30 days of the date of this inspection report,

with the basis for your disagreement, to the Regional Administrator, Region IV, and the NRC

Resident Inspector at San Onofre Nuclear Generating Station. The information you provide will

be considered in accordance with Inspection Manual Chapter 0305.

Southern California Edison Company -2-

In accordance with 10 CFR 2.390 of the NRC's Rules of Practice, a copy of this letter, and its

enclosure, will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records component of NRCs document system (ADAMS).

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the

Public Electronic Reading Room).

Sincerely,

/RA/

Ryan E. Lantz, Chief

Project Branch D

Division of Reactor Projects

Docket Nos. 50-361

50-362

License Nos. NPF-10 NPF-15

Enclosure:

NRC Inspection Report 05000361/2009005 and 05000362/2009005

w/Attachment: Supplemental Information

Distribution:

See next page

Southern California Edison Company -3-

cc w/Enclosure: James D. Boyd, Commissioner

Chairman, Board of Supervisors California Energy Commission

County of San Diego 1516 Ninth Street (MS 34)

1600 Pacific Highway, Room 335 Sacramento, CA 95814

San Diego, CA 92101

Douglas K. Porter, Esq.

Gary L. Nolff Southern California Edison Company

Assistant Director-Resources 2244 Walnut Grove Avenue

City of Riverside Rosemead, CA 91770

3900 Main Street

Riverside, CA 92522 Albert R. Hochevar

Southern California Edison Company

Mark L. Parsons San Onofre Nuclear Generating Station

Deputy City Attorney P.O. Box 128

City of Riverside San Clemente, CA 92675

3900 Main Street

Riverside, CA 92522 Steve Hsu

Department of Health Services

Gary H. Yamamoto, P.E., Chief Radiologic Health Branch

Division of Drinking Water and MS 7610, P.O. Box 997414

Environmental Management Sacramento, CA 95899-7414

1616 Capitol Avenue, MS 7400

P.O. Box 997377 R. St. Onge

Sacramento, CA 95899-7377 Southern California Edison Company

San Onofre Nuclear Generating Station

Michael J. DeMarco P.O. Box 128

San Onofre Liaison San Clemente, CA 92674-0128

San Diego Gas & Electric Company

8315 Century Park Ct. CP21C Chief, Technological Hazards Branch

San Diego, CA 92123-1548 FEMA Region IX

1111 Broadway, Suite 1200

Director, Radiological Health Branch Oakland, CA 94607-4052

State Department of Health Services

P.O. Box 997414 (MS 7610) Chairperson, Radiological Assistance

Sacramento, CA 95899-7414 Committee

Region IX

Mayor Federal Emergency Management Agency

City of San Clemente Department of Homeland Security

100 Avenida Presidio 1111 Broadway, Suite 1200

San Clemente, CA 92672 Oakland, CA 94607-4052

Southern California Edison Company -4-

Electronic distribution by RIV:

Regional Administrator (Elmo.Collins@nrc.gov)

Deputy Regional Administrator (Chuck.Casto@nrc.gov)

DRP Director (Dwight.Chamberlain@nrc.gov)

DRP Deputy Director (Anton.Vegel@nrc.gov)

DRS Director (Roy.Caniano@nrc.gov)

DRS Deputy Director (Troy.Pruett@nrc.gov)

Senior Resident Inspector (Greg.Warnick@nrc.gov)

Resident Inspector (John.Reynoso@nrc.gov)

Branch Chief, DRP/D (Ryan.Lantz@nrc.gov)

Senior Project Engineer, DRP/D (Don.Allen@nrc.gov)

SONGS Administrative Assistant (Heather.Hutchinson@nrc.gov)

Public Affairs Officer (Victor.Dricks@nrc.gov)

Public Affairs Officer (Lara.Uselding@nrc.gov)

Branch Chief, DRS/TSB (Michael.Hay@nrc.gov)

RITS Coordinator (Marisa.Herrera@nrc.gov)

Regional Counsel (Karla.Fuller@nrc.gov)

Congressional Affairs Officer (Jenny.Weil@nrc.gov)

OEMail Resource

ROPreports

DRS/TSB STA (Dale.Powers@nrc.gov)

OEDO RIV Coordinator (Leigh.Trocine@nrc.gov)

Regional State Liaison Officer (Bill.Maier@nrc.gov)

NSIR/DPR/EP (Eric.Schrader@nrc.gov)

NSIR/DPR/EP (Steve.LaVie@nrc.gov)

File located: R:\Reactors\Songs\SO2009005-RP-GGW.doc ADAMS ML

SUNSI Rev Compl. ; Yes No ADAMS  ; Yes No Reviewer Initials RL

Publicly Avail  ; Yes No Sensitive Yes ; No Sens. Type Initials RL

C:DRS/EB2 C:DRS/PSB2 C:DRS/EB1 C:DRS/OB C:DRS/PSB1

NO'Keefe GWerner TFarnholtz MHaire MShannon

/RA/ /RA/ /RA/ /RA/ /RA/

2/1/10 2/1/10 1/29/10 1/28/10 2/1/10

C:DRP SRI:Songs

RLantz GWarnick

/RA/ /RA/

2/10/10 2/10/10

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 50-361, 50-362

License: NPF-10, NPF-15

Report: 05000361/2009005 and 05000362/2009005

Licensee: Southern California Edison Co. (SCE)

Facility: San Onofre Nuclear Generating Station, Units 2 and 3

Location: 5000 S. Pacific Coast Hwy

San Clemente, California

Dates: September 24, 2009 through December 31, 2009

Inspectors: J. Adams, Reactor Inspector

M. Bloodgood, Reactor Inspector

P. Elkmann, Senior Emergency Preparedness Inspector

A. Fairbanks, Reactor Inspector

G. Guerra, CHP, Emergency Preparedness Inspector

C. Osterholtz, Senior Operations Engineer

C. Proctor, General Scientist

J. Reynoso, Resident Inspector

L. Ricketson, Senior Health Physicist

R. Schmitt, Emergency Preparedness Specialist

G. Warnick, Senior Resident Inspector

Approved By: Ryan Lantz, Chief,

Project Branch D

Division of Reactor Projects

-1- Enclosure

SUMMARY OF FINDINGS

IR 05000361/2009005, 05000362/2009005; 09/24/2009 - 12/31/2009; San Onofre Nuclear

Generating Station, Units 2 & 3, Integrated Resident and Regional Report; Flood Prot. Meas.,

Maint. Effect., Operability Evaluations, Event Follow-up, & Other Activities.

The report covered a 3-month period of inspection by resident inspectors and announced

baseline inspections by regional based inspectors. Eight noncited violations and two findings of

significance were identified. The significance of most findings is indicated by their color (Green,

White, Yellow, or Red) using Inspection Manual Chapter 0609, Significance Determination

Process. Findings for which the significance determination process does not apply may be

Green or be assigned a severity level after NRC management review. The NRC's program for

overseeing the safe operation of commercial nuclear power reactors is described in NUREG-

1649, Reactor Oversight Process, Revision 4, dated December 2006.

A. NRC-Identified Findings and Self-Revealing Findings

Cornerstone: Initiating Events

  • Green. The inspectors identified a finding for the failure of maintenance

personnel to use the standards described in Procedure SO23-XV-2,

Troubleshooting Plant Equipment and Systems, in developing procedures and

work plans to adequately perform, test, and communicate maintenance activities

on Unit 2 circulating water gate 5. Specifically, from September 5 through

September 13, 2009, maintenance personnel did not have adequate procedures

in place to perform corrective maintenance on Unit 2 circulating water gate 5.

The attempts to repair gate 5 were repeatedly unsuccessful due to inadequate

planning, execution, postmaintenance testing, and communication. This finding

was entered into the licensees corrective action program as Nuclear Notifications

NNs 200580999 and 200718204.

The finding is greater than minor because the performance deficiency was a

precursor to a significant event (reactor trip). Using the Manual Chapter 0609,

Significance Determination Process, Phase 1 Worksheets, the finding is

determined to have very low safety significance because the finding did not

contribute to both the likelihood of a reactor trip and the likelihood that mitigation

equipment or functions would not be available. The finding has a crosscutting

aspect in the area of human performance associated with work control because

maintenance personnel failed to incorporate actions to address the need for work

groups to communicate, coordinate, and cooperate with each other during

activities in which interdepartmental coordination is necessary to assure plant

and human performance H.3(b) (Section 4OA3).

  • Green. The inspectors identified a finding for the failure of operations personnel

to perform an adequate pre-job brief in accordance with procedural requirements

for a planned Unit 2 heat treat evolution. Specifically, on September 13, 2009,

operations personnel failed to provide a thorough pre-job brief in preparation for

the performance of the heat treat evolution which contributed to a delay in

operator actions which ultimately resulted in a turbine and reactor trip on low

condenser vacuum due to escalated circulating water temperatures. This finding

-2- Enclosure

was entered into the licensees corrective action program as Nuclear Notification

NN 200580999.

The finding is greater than minor because the performance deficiency was a

precursor to a significant event (reactor trip). Using the Manual Chapter 0609,

Significance Determination Process, Phase 1 Worksheets, the finding is

determined to have very low safety significance because the finding did not

contribute to both the likelihood of a reactor trip and the likelihood that mitigation

equipment or functions would not be available. The finding has a crosscutting

aspect in the area of human performance associated with resources because the

licensee failed to provide adequate procedural guidance to ensure that

operations personnel could safely perform plant evolutions H.2(c)

(Section 4OA3).

  • Green. Three examples of a self-revealing noncited violation of Technical

Specification 5.5.1.1.d, was identified for the failure of contractor personnel to

properly implement the requirements of a fire protection procedure for the control

of hot work activities. Specifically, between September 1 and 29, 2009, three

examples were identified where contractor personnel failed to properly implement

the requirements of Procedure SO123-XV-1.41, Steps 6.1.1 and 6.4.1.3, in that,

combustible materials were not covered or stored at a distance of 35 feet from

the ignition source or flame, and no evaluation was performed. This finding was

entered into the licensees corrective action program as Nuclear Notification NN

200604378.

The finding is greater than minor because it is associated with the protection

against external factors (fires) attribute of the Initiating Events Cornerstone and

affects the cornerstone objective to limit the likelihood of those events that upset

plant stability and challenge critical safety functions during shutdown as well as

power operations. Additionally, if left uncorrected, the practice of conducting hot

work in a manner that results in unintended combustion of nearby materials

would have the potential to lead to a more significant safety concern in that it

could result in a fire in or near risk significant equipment. Manual Chapter 0609,

Appendix M, Significance Determination Process Using Qualitative Criteria, was

used since Appendix F, Fire Protection Significance Determination Process,

does not address the potential risk significance of shutdown fire protection

findings, and Appendix G, Shutdown Operations Significance Determination

Process, does not address fire protection findings. The NRC management

review was performed by using the Manual Chapter 0609, Appendix F, Phase 1

Worksheet, to establish a bounding analysis. Using the bounding analysis, the

finding is determined to have very low safety significance because the finding

represented a low degradation rating, in that, it did not have any significant effect

on the likelihood that a fire might occur, or that a fire which does occur might not

be promptly suppressed. This finding has a crosscutting aspect in the area of

human performance associated with work practices because the licensee failed

to ensure supervisory and management oversight of work activities, including

contractors, such that nuclear safety was supported H.4(c) (Section 4OA3).

Cornerstone: Mitigating Systems

-3- Enclosure

Appendix B, Criterion V, Instructions, Procedures, Drawings, for the failure of

operations personnel to initiate a nuclear notification within the required

timeframe. Specifically, on September 27, 2009, operations personnel failed to

write a nuclear notification to document the problem with a flooded auxiliary

feedwater vault prior to the end of their shift. This finding was entered into the

licensees corrective action program as Nuclear Notifications NN 200615922.

The finding is greater than minor because the failure to follow procedures for

writing nuclear notifications, if left uncorrected, would have the potential to lead to

a more significant safety concern. The finding is associated with the equipment

performance attribute of the Mitigating Systems Cornerstone and affects the

cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

Using the Manual Chapter 0609, Significance Determination Process, Phase 1

Worksheets, the finding is determined to have very low safety significance

because the finding did not result in an actual loss of safety function, and did not

screen as potentially risk significant due to a seismic, flooding, or severe weather

initiating event. This finding has a crosscutting aspect in the area of problem

identification and resolution associated with corrective action program since the

licensee failed to implement the corrective action program with an appropriate

threshold for identified issues P.1(a) (Section 1R06).

Appendix B, Criterion XVI, Corrective Action, for failure of engineering

personnel to adequately identify for correction conditions adverse to quality

between November 10 and December 1, 2009. Specifically, the inspection of

potential degradation associated with the support welds and embedded wall

plates for safety related seismic pipe restraints for emergency core cooling piping

was inadequate, in that, standing water and corrosion product interference was

not removed to enable an adequate inspection and evaluation of the structural

material. This finding was entered into the licensees corrective action program

as Nuclear Notification NN 200743417.

The finding is greater than minor because the failure to adequately identify for

correction conditions adverse to quality on safety related equipment, if left

uncorrected, would have the potential to lead to a more significant safety

concern. Additionally, the finding is associated with the equipment performance

attribute of the Mitigating Systems Cornerstone and affects the cornerstone

objective to ensure the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences. Using the

Manual Chapter 0609, Significance Determination Process, Phase 1

Worksheets, the finding is determined to have very low safety significance

because it did not represent an actual loss of safety function, and did not screen

as potentially risk significant due to a seismic, flooding, or severe weather

initiating event. The finding has a crosscutting aspect in the area of human

performance associated with decision making because engineering personnel

failed to use conservative assumptions for operability decision making when

inspecting degraded and nonconforming conditions H.1(b) (Section 1R06).

-4- Enclosure

Appendix B, Criterion XVI, Corrective Action, for the licensee's failure to take

adequate corrective actions for conditions adverse to quality associated with

Unit 3 emergency diesel generator train B. Specifically, in May 2009, corrective

actions were inadequate following an unexpected fuse failure in the emergency

diesel generator train B annunciator system. These inadequate corrective

actions enabled the pre-existing ground condition to continue until it ultimately

rendered the emergency diesel generator train B inoperable on December 11,

2009. This finding was entered into the licensees corrective action program as

Nuclear Notification NN 200722170.

The finding is greater than minor because the failure to correct conditions

adverse to quality for the emergency diesel generators is associated with the

equipment performance attribute of the Mitigating Systems Cornerstone and

affects the associated cornerstone objective to ensure the availability, reliability,

and capability of systems that respond to initiating events to prevent undesirable

consequences. Using the Manual Chapter 0609, Significance Determination

Process, Phase 1 Worksheets, the finding is determined to have very low safety

significance because it did not represent an actual loss of safety function, and did

not screen as potentially risk significant due to a seismic, flooding, or severe

weather initiating event. This finding has a crosscutting aspect in the area of

problem identification and resolution associated with corrective action program

since the licensee failed to thoroughly evaluate problems such that the

resolutions address the causes and extent of conditions P.1(c) (Section 1R12).

Appendix B, Criterion XVI, Corrective Action, for the licensee's failure to take

adequate corrective actions for conditions adverse to quality associated with

Unit 3 emergency diesel generator train A. Specifically, on June 13, 2009,

following an emergency diesel generator failure on June 6, 2009, immediate

corrective actions were inadequately implemented when improperly configured

annunciator power supplies were installed in the emergency diesel generator

train A annunciator system. This configuration problem contributed to rapid

capacitor degradation as a result of the increased heat from a resistor, which

ultimately caused the emergency diesel generator failure to start on

December 12, 2009. This finding was entered into the licensees corrective

action program as Nuclear Notification NN 200756001.

The finding is greater than minor because the failure to correct conditions

adverse to quality for the emergency diesel generators is associated with the

equipment performance attribute of the Mitigating Systems Cornerstone and

affects the associated cornerstone objective to ensure the availability, reliability,

and capability of systems that respond to initiating events to prevent undesirable

consequences. Using the Manual Chapter 0609, Significance Determination

Process, Phase 1 Worksheets, the inspectors determined that this finding

represented an actual loss of safety function of emergency diesel generator train

for greater than the technical specification allowed outage time. This required

that a Phase 2 estimation be completed. Because the Phase 2 analysis

concluded that the finding was potentially greater than green, a Phase 3 analysis

was completed by a regional senior reactor analyst. The San Onofre SPAR

model indicated that the delta core damage frequency for emergency diesel

-5- Enclosure

generator train A being non-functional was 2.0E-6/yr. For an exposure time of

7 days, this resulted in an incremental core damage frequency of 3.8E-8 for this

finding, considering internal events only. The dominant sequence was a station

blackout sequence with failure of the diesels, failure to cross-tie power from the

other unit, failure to recover either onsite or offsite power, failure of batteries at

4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, and a failure to manually control the turbine-driven auxiliary feedwater

pump after battery depletion. The senior reactor analyst determined qualitatively

that the contribution of external events would not significantly add to this result;

therefore, the finding is determined to be of very low safety significance. This

finding has a crosscutting aspect in the area of human performance associated

with resources because the licensee failed to provide adequate instructions to

perform activities affecting quality H.2(c) (Section 1R12).

  • Green. The inspectors identified three examples of a noncited violation of

10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures and

Drawings, for the failure of operations and engineering personnel to follow

procedures and adequately evaluate degraded conditions to support operability

decision making. Specifically, on October 29, 2009, engineering personnel failed

to adequately evaluate the operability of the Unit 3 containment emergency sump

when an unanalyzed styrofoam material was identified, which had not been

previously analyzed for impact to the containment emergency sump.

Additionally, on November 17 and December 18, 2009, operations and

engineering personnel failed to adequately evaluate the operability of emergency

diesel generator train B when a lube oil leak was identified on a flexible hose for

the dc auxiliary turbo pump. And finally, on December 19, 2009, operations and

engineering personnel inappropriately applied Code Case N-513-2 to justify the

operability of the emergency core cooling system train A, in that, the flaw

geometry was only assumed and not characterized by volumetric inspection

methods or by physical measurements. This finding was entered into the

licensees corrective action program as Nuclear Notifications NNs 200673198,

200699833, and 200718673.

The finding is greater than minor because the failure to perform timely and

adequate evaluations of degraded, nonconforming, and unanalyzed conditions

for operability, if left uncorrected, would have the potential to lead to a more

significant safety concern. The finding is associated with the equipment

performance attribute of the Mitigating Systems Cornerstone and affects the

associated cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. Using the Manual Chapter 0609, Significance Determination

Process, Phase 1 Worksheets, the finding is determined to have very low safety

significance because the finding did not result in a loss of safety function for

greater than the technical specification allowed outage time, and did not screen

as potentially risk significant due to a seismic, flooding, or severe weather

initiating event. This finding has a crosscutting aspect in the area of problem

identification and resolution associated with corrective action program because

operations and engineering personnel failed to thoroughly evaluate problems

such that the resolutions addressed the cause and extent of condition. This

includes properly classifying, prioritizing, and evaluating for operability conditions

adverse to quality P.1(c) (Section 1R15).

-6- Enclosure

Appendix B, Criterion V, Instructions, Procedures and Drawings, for the failure

of operations personnel to follow procedures and adequately implement identified

compensatory measures. Specifically, on November 25 and 28, 2009,

operations personnel did not follow requirements to establish a compensatory

measure to substitute manual operator actions for automatic actions to support

the operability of the functions provided by the refueling water storage tank to

charging pump suction piping. This finding was entered into the licensees

corrective action program as Nuclear Notification NN 200689450.

The finding is greater than minor because the inadequate implementation of

compensatory measures, if left uncorrected, would have the potential to lead to a

more significant safety concern. The finding is associated with the procedure

quality attribute of the Mitigating Systems Cornerstone and affects the associated

cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

Using the Manual Chapter 0609, Significance Determination Process, Phase 1

Worksheets, the finding is determined to have very low safety significance

because the finding did not result in an actual loss of safety function, and did not

screen as potentially risk significant due to a seismic, flooding, or severe weather

initiating event. This finding has a crosscutting aspect in the area of human

performance associated with decision making because operations personnel

failed to make decisions using a systematic process, especially when faced with

uncertain or unexpected plant conditions, to ensure safety is maintained H.1(a)

(Section 1R15).

Appendix B, Criterion III, Design Control, with thirteen examples that occurred

between June 2005 and July 2008, for the failure of the licensee to ensure that

appropriate measures were in place to assure that systems specified in the

design basis were maintained in a configuration which provided a reasonable

assurance of operability during design basis events. This finding was entered

into the licensees corrective action program as Action Requests ARs 050601315,

050601324, 060101159, 070200254, 200066209, and Nuclear Notifications NNs

200089167, 200058371, 200100730, and Corrective Action Order 800126624.

The finding is greater than minor because it is associated with the equipment

performance attribute of the Mitigating Systems Cornerstone and affects the

associated cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. In accordance with Manual Chapter 0609, Attachment 4,

Table 4a, Question 5, a Phase 3 analysis was required because the finding

screened as potentially risk significant due to a seismic, flooding, or severe

weather initiating event. In accordance with Inspection Manual Chapter 0609,

Appendix A, the analyst determined that the conditions documented in Table 1 of

this inspection report should be evaluated as a single inspection finding because

they resulted from a common cause. As a combined result of the evaluations

performed in the Phase 3 analysis, the analyst determined that this finding was of

very low safety significance. The finding has a crosscutting aspect in the area of

human performance associated with resources for the failure to maintain

-7- Enclosure

complete, accurate, and up-to-date design documentation, procedures, and work

packages H.2(c) (Section 4OA5).

B. Licensee-Identified Violations

Violations of very low safety significance, which were identified by the licensee, have

been reviewed by the inspectors. Corrective actions taken or planned by the licensee

have been entered into the licensees corrective action program. These violations and

their associated corrective action tracking numbers are listed in Section 4OA7.

-8- Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 2 began the inspection period at full power. On September 27, 2009, the unit was

shutdown for a scheduled refueling outage (U2C16) and steam generator replacement.

Unit 3 began the inspection period at full power. On October 24, 2009, the unit reduced power

to investigate an electrical ground on the high pressure intercept valves and during the

troubleshooting activities a valve (UV2200E) inadvertently closed resulting in a power reduction

to 88 percent. After repairs, the unit returned to full power on October 25, 2009. On

December 12, 2009, the unit commenced a technical specification required shutdown due to

both trains of emergency diesel generators being declared inoperable. The unit reduced power

to 40 percent before recovery of one train of emergency diesel generators allowed the unit to

exit the technical specification action and return to full power. The unit returned to full power on

December 13, 2009, and remained there for the duration of the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

Readiness for Seasonal Extreme Weather Conditions

a. Inspection Scope

The inspectors performed a review of the licensees adverse weather procedures for

seasonal extremes (e.g., extreme high temperatures, extreme low temperatures, or

hurricane season preparations). The inspectors verified that weather-related equipment

deficiencies identified during the previous year were corrected prior to the onset of

seasonal extremes; and evaluated the implementation of the adverse weather

preparation procedures and compensatory measures for the affected conditions before

the onset of, and during, the adverse weather conditions.

During the inspection, the inspectors focused on plant-specific design features and the

licensees procedures used to mitigate or respond to adverse weather conditions.

Additionally, the inspectors reviewed the Updated Final Safety Analysis Report and

performance requirements for systems selected for inspection, and verified that operator

actions were appropriate as specified by plant-specific procedures. Specific documents

reviewed during this inspection are listed in the attachment. The inspectors also

reviewed corrective action program items to verify that the licensee was identifying

adverse weather issues at an appropriate threshold and entering them into their

corrective action program in accordance with station corrective action procedures. The

inspectors reviews focused specifically on the following plant systems:

  • December 7-8, 2009, Units 2 and 3, the inspectors completed a review of the

licensee's readiness of the condensate storage tank and auxiliary feedwater

system for extreme low temperatures

These activities constitute completion of one readiness for seasonal adverse weather

sample as defined in IP 71111.01-05.

-9- Enclosure

b. Findings

No findings of significance were identified.

1R04 Equipment Alignments (71111.04)

.1 Partial Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

  • December 8, 2009, Unit 3, Class 1E 4 kV bus (3A04 and 3A06) supply breakers

while emergency diesel generator train B was out of service for maintenance

  • December 23, 2009, Unit 2, saltwater cooling system train B

The inspectors selected these systems based on their risk significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could affect the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, Updated Final Safety Analysis Report, technical specification

requirements, administrative technical specifications, outstanding work orders, condition

reports, and the impact of ongoing work activities on redundant trains of equipment in

order to identify conditions that could have rendered the systems incapable of

performing their intended functions. The inspectors also walked down accessible

portions of the systems to verify system components and support equipment were

aligned correctly and operable. The inspectors examined the material condition of the

components and observed operating parameters of equipment to verify that there were

no obvious deficiencies. The inspectors also verified that the licensee had properly

identified and resolved equipment alignment problems that could cause initiating events

or impact the capability of mitigating systems or barriers and entered them into the

corrective action program with the appropriate significance characterization. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of three partial system walkdown samples as

defined by IP 71111.04-05.

b. Findings

No findings of significance were identified.

.2 Semi-Annual Complete Walkdown

a. Inspection Scope

On October 16, 2009, the inspectors performed a complete system alignment inspection

of the spent fuel pool cooling system to verify the functional capability of the system.

The inspectors selected this system because it was considered both safety-significant

and risk-significant in the licensees probabilistic risk assessment. The inspectors

- 10 - Enclosure

walked down the system to review mechanical and electrical equipment line ups,

electrical power availability, system pressure and temperature indications, as

appropriate, component labeling, component lubrication, component and equipment

cooling, hangers and supports, operability of support systems, and to ensure that

ancillary equipment or debris did not interfere with equipment operation. The inspectors

reviewed a sample of past and outstanding work orders to determine whether any

deficiencies significantly affected the system function. In addition, the inspectors

reviewed the corrective action program database to ensure that system equipment-

alignment problems were being identified and appropriately resolved. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one complete system walkdown sample as

defined by IP 71111.04-05.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

Quarterly Fire Inspection Tours

a. Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

  • October 1, 2009, Unit 2, containment building elevations 20 foot through 68 foot
  • November 9, 2009, Unit 2, hot work activities in steam generator E088 cubicle
  • December 4, 2009, Unit 2, saltwater cooling pump room and pipe tunnel
  • December 8, 2009, Units 2 and 3, fire water pumps and storage tanks
  • December 9-11, 2009, Units 2 and 3, auxiliary control building 9, 50, 70, and

85 feet elevations

The inspectors reviewed areas to assess if licensee personnel had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant; effectively maintained fire detection and suppression capability; maintained

passive fire protection features in good material condition; and had implemented

adequate compensatory measures for out of service, degraded or inoperable fire

protection equipment, systems, or features, in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to affect equipment that could initiate or mitigate a plant

transient, or their impact on the plants ability to respond to a security event. Using the

documents listed in the attachment, the inspectors verified that fire hoses and

extinguishers were in their designated locations and available for immediate use; that

fire detectors and sprinklers were unobstructed, that transient material loading was

- 11 - Enclosure

within the analyzed limits; and fire doors, dampers, and penetration seals appeared to

be in satisfactory condition. The inspectors also verified that minor issues identified

during the inspection were entered into the licensees corrective action program.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of five quarterly fire-protection inspection samples

as defined by IP 71111.05-05.

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures (71111.06)

a. Inspection Scope

The inspectors reviewed the Updated Final Safety Analysis Report, the flooding analysis,

and plant procedures to assess seasonal susceptibilities involving internal flooding;

reviewed the Updated Final Safety Analysis Report and corrective action program to

determine if licensee personnel identified and corrected flooding problems; inspected

underground bunkers/manholes to verify the adequacy of sump pumps, level alarm

circuits, cable splices subject to submergence, and drainage for bunkers/manholes;

verified that operator actions for coping with flooding can reasonably achieve the desired

outcomes; and walked down the areas listed below to verify the adequacy of equipment

seals located below the flood line, floor and wall penetration seals, watertight door seals,

common drain lines and sumps, sump pumps, level alarms, and control circuits, and

temporary or removable flood barriers. Specific documents reviewed during this

inspection are listed in the attachment.

room inspections

equipment building

and safety related equipment in the auxiliary control building

These activities constitute completion of one internal flooding and one review of cables

located in underground bunkers/manholes inspection samples as defined by

IP 71111.06-05.

b. Findings

1. Timely Initiation for Nuclear Notifications

Introduction. The inspectors identified a Green noncited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, Drawings, for the failure of

operations personnel to initiate a nuclear notification within the required timeframe.

Description. On September 29, 2009, when Unit 2 was in Mode 5, the inspectors

identified three inches of standing water in an electrical vault located on the southeast

- 12 - Enclosure

side of the auxiliary feedwater building. The inspectors observed the vault contained

underground electrical conduit to safety related auxiliary feedwater pump 2P504.

Operations control room personnel were immediately notified of the condition and

Nuclear Notification NN 200602405 was initiated. Operations personnel identified that

the flooded condition was identified two days earlier on September 27, 2009, by an

equipment operator. However, no nuclear notification had been initiated as required by

Procedure SO123-XV-50.CAP-1, Writing Nuclear Notification for Problem Identification

and Resolution, Revision 2. Procedure SO123-XV-50.CAP-1, Section 6.3, stated that

all personnel identifying problems that have the potential to affect the ability of a

structure, system, or component to perform its specified function will immediately notify

the shift manager or designee, and write a nuclear notification prior to the end of their

shift.

Engineering personnel inspected the vault and surrounding areas on September 29-30,

2009, to determine the source of the flooding. Adjacent to the auxiliary feedwater

building, water was located in the berm surrounding the nuclear service water tanks and

pumps. The reported source of the water was from a drain valve connected to the floor

drain from the condensate storage tank T121 room. The water in the nuclear service

water berm was found to be entering a degraded underground electrical conduit for a

nuclear service water pump. The water entered into the conduit and traveled down to

the cable tray located in the auxiliary feedwater vault.

The inspectors determined this degraded condition was not promptly entered into the

correction action program until identified by the inspectors. The safety related

equipment components associated with the vault were not immediately evaluated for

operability when the condition was entered into the corrective action program on

September 29, 2009, because the auxiliary feedwater system was not required to be

operable in Mode 5. The inspectors concluded that, because of the failure to follow

Procedure SO123-XV-50.CAP-1, an appropriate immediate operability determination of

safety related equipment was not done, while in the applicable mode, since the

degraded or flooded condition of the auxiliary feedwater vault was first discovered on

September 27, 2009, while the unit was still in Mode 3.

Based on the inspectors prompting on October 8, 2009, the licensee initiated Nuclear

Notification NN 200615922 to document the failure to write a nuclear notification for a

degraded condition which required an immediate operability determination.

The inspectors reviewed an additional example identified by the licensee (See

Section 4OA7.3) that occurred on November 20, 2009, when engineering personnel

observed a white deposit on Unit 2 pipe S21219ML057, T006 RWST Gravity Feed

Outlet, during an inspection of the auxiliary feedwater line tunnel. The engineer initially

thought that the pipe was part of the condensate system and did not warrant an

immediate nuclear notification. The engineer noted the deficiency and took a picture

which included the date and time.

On November 23, 2009, the original engineer showed the picture to another system

engineer for evaluation. The second engineer routinely performed inspection for boric

acid and discussed the possibility of the white substance as being boric acid with the

original engineer. The discussion concluded that the substance was probably boric acid

from an external source and that the piping was suspected to be part of the condensate

system. Neither of the engineers identified the need to initiate a nuclear notification in

- 13 - Enclosure

accordance Procedure SO123-XV-50.CAP-1. Further, the engineers failed to recognize

the condition as a problem that warranted a nuclear notification as required by

Procedure SO23-XV-85, Boric Acid Corrosion Control Program (BACCP), Revision 4.

Procedure SO23-XV-85 stated that, all boric acid leaks, including minor amounts of

residue, require a nuclear notification be initiated. At this time the engineers arranged

for another walk down which did not occur until November 25, 2009.

On November 25, 2009, both of the engineers performed an additional inspection of the

auxiliary feedwater tunnel to identify the source of the white deposit. Due to suspecting

that the substance was boric acid, prior to the inspection the engineers arranged for a

sample of the white substance to be obtained and analyzed. Additionally, the engineers

identified that the piping was associated with the refueling water storage tank and

determined that the deposit was likely boric acid. Following the additional inspection, the

engineers reported the condition to their supervisor who appropriately directed the

engineers to immediately notify the operations shift manager and initiate a nuclear

notification. The condition was documented on Nuclear Notification NN 200682817.

During the discussion, the engineering supervisor was not informed that the boric acid

leak was initially identified on November 20, 2009, which was five days earlier.

Following shift manager notification, an extent of condition review was performed on

Unit 3 which identified three additional boric acid leaks on similar piping, which resulted

in the entry into a one hour technical specification shutdown action statement.

On November 27, 2009, the engineering supervisor observed the picture of the boric

acid leak and noted that the picture was dated November 20, 2009. Noting the

discrepancy between the time that the condition was identified and the time that the

condition was entered into the corrective action program, the engineering supervisor

identified that the requirements of Procedure SO123-XV-50.CAP-1 were not followed.

The engineering supervisor initiated Nuclear Notification NN 200683697 to document the

failure to promptly initiate a nuclear notification.

Analysis. The failure to initiate a nuclear notification in a timely manner following the

identification of an equipment problem was a performance deficiency. The finding is

greater than minor because the failure to follow procedures for writing nuclear

notifications, if left uncorrected, would have the potential to lead to a more significant

safety concern. The finding is associated with the equipment performance attribute of

the Mitigating Systems Cornerstone and affects the cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences. Using the Manual Chapter 0609, Significance

Determination Process, Phase 1 Worksheets, the finding is determined to have very low

safety significance because the finding did not result in an actual loss of safety function,

and did not screen as potentially risk significant due to a seismic, flooding, or severe

weather initiating event. This finding has a crosscutting aspect in the area of problem

identification and resolution associated with corrective action program since the licensee

failed to implement the corrective action program with an appropriate threshold for

identified issues P.1(a).

Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, states, in part, that activities

affecting quality shall be prescribed by documented instructions, procedures, or

drawings, of a type appropriate to the circumstances and shall be accomplished in

accordance with these instructions, procedures, or drawings. Procedure SO123-XV-

- 14 - Enclosure

50.CAP-1, Writing Nuclear Notifications for Problem Identification and Resolution,

Revision 2, stated that all personnel identifying problems that have the potential to affect

the ability of a structure, system, or component to perform its specified function will

immediately notify the shift manager or designee, and write a nuclear notification prior to

the end of their shift. Contrary to the above, on September 27, 2009, operations

personnel failed to write a nuclear notification to document the problem with a flooded

auxiliary feedwater vault prior to the end of their shift. As a result, an immediate

operability determination, as required by Procedure SO123-XV-52, Functionality

Assessment and Operability Determinations, Revision 13, was not completed in a timely

manner. Because this violation is of very low safety significance and has been entered

into the licensee's corrective action program as Nuclear Notification NN 200615922, this

violation is being treated as a noncited violation, consistent with Section VI.A of the NRC

Enforcement Policy: NCV 05000361/2009005-01, Failure to Initiate a Notification in a

Timely Manner.

2. Pipe Support Material Degradation

Introduction. The inspectors identified a Green noncited violation of 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, for failure of engineering personnel to

adequately identify for correction conditions adverse to quality between November 10

and December 1, 2009. Specifically, engineering personnel did not adequately inspect

degraded safety related seismic pipe supports exposed to ground water in the Unit 2

auxiliary feedwater tunnel to identify all actions necessary to evaluate and correct the

condition.

Description. Between November 10 and December 1, 2009, inspectors performed

walkdowns of Unit 2 auxiliary feedwater piping underground tunnel. Degraded piping

penetrations between the safety equipment building room and auxiliary feedwater tunnel

areas was identified as a long standing issue by NRC inspectors (NCV

05000361/2009004-01). The degraded seal allowed ground water to leak into the safety

equipment building for several years. Two trains of the emergency core cooling system

piping pass through the auxiliary feedwater piping tunnel into the safety equipment

building. The inspectors were informed that repairs to the penetration seals on the

safety equipment building side had been completed. In order to verify the condition of

the piping penetration on both sides, inspectors requested entry to the auxiliary

feedwater piping tunnel. This was necessary to evaluate the general condition of the

piping penetration seals in the tunnel and determine the impact water leakage had on

safety related equipment in the auxiliary feedwater tunnel. Access was restricted to the

piping tunnel by a locked door and required a radiation exposure permit before entry.

The inspectors noted that water was discovered in the tunnel by a health physics

technician during a routine health physics survey on November 8, 2009. The technician

generated Nuclear Notification NN 200659260, and according to the description, water

was present in the tunnel during the previous surveillance and needed to be pumped

down. The inspectors questioned the licensee regarding how often water had been

found in the tunnel since the last health physic survey, but no recent documented

occurrences were identified in the corrective action program.

During the piping tunnel inspection, the inspectors observed that the flooding was due to

leaking seals from degraded wall penetrations between the safety equipment building

and the auxiliary feedwater tunnel. The inspectors observed that the groundwater had

- 15 - Enclosure

affected emergency core cooling system pipe supports trains A and B as evidenced by

heavy rust at the base of the supports. On November 17, 2009, the licensee

documented the inspectors observations in Nuclear Notification NN 200670710, which

included the pipe support degradation concerns.

Since the piping supports are embedded in the tunnel floor, they have been repeatedly

exposed to standing water for extended periods of time. On November 18, 2009,

engineering personnel inspected the piping support welds and embedded wall plates for

corrosion, to identify potential material degradation, as directed per Nuclear Notification

NN 200670710. Engineering personnel concluded that the corrosion on the supports

and welds appeared to be minor surface corrosion, such that the structural material was

not impacted. Therefore, it was concluded that no further evaluation was required since

the corrosion did not impact structural integrity of the supports. The corrective action

identified was to clean and repaint the corroded pipe support areas to prevent further

degradation.

On December 1, 2009, inspectors returned to the piping tunnel with engineering

personnel and observed that the corroded pipe supports appeared to be in the same

condition that was observed during their previous inspection. Further, the inspectors

were informed that the pipe support inspection was performed by visual examination of

the conditions that the inspectors observed. The inspectors questioned engineering

personnel how an adequate inspection of the condition was performed without the

removal of standing water and corrosion, since the interference would obstruct an

adequate view of the material surface that needed to be evaluated. In response to the

inspectors question, engineering personnel initiated action for additional pipe support

inspections that would require removal of interference to adequately inspect the pipe

support structural materials.

On December 18, 2009, the results of the additional inspection and evaluation were

presented to the inspectors. The results confirmed the inspectors concerns that some

of the pipe support welds had sustained material degradation, which was more than

minor surface corrosion. The engineering analyses to justify the degradation showed a

loss of margin in various piping welds but the support strength remained within allowable

design limits.

Analysis. The failure to adequately identify for correction conditions adverse to quality

was a performance deficiency. The finding is greater than minor because the failure to

adequately identify for correction conditions adverse to quality on safety related

equipment, if left uncorrected, would have the potential to lead to a more significant

safety concern. Additionally, the finding is associated with the equipment performance

attribute of the Mitigating Systems Cornerstone and affects the cornerstone objective to

ensure the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. Using the Manual Chapter 0609,

Significance Determination Process, Phase 1 Worksheets, the finding is determined to

have very low safety significance because it did not represent an actual loss of safety

function, and did not screen as potentially risk significant due to a seismic, flooding, or

severe weather initiating event. The finding has a crosscutting aspect in the area of

human performance associated with decision making because engineering personnel

failed to use conservative assumptions for operability decision making when inspecting

degraded and nonconforming conditions H.1(b).

- 16 - Enclosure

Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,

Criterion XVI, Corrective Action, requires, in part, that measures shall be established to

assure that conditions adverse to quality, such as failures, malfunctions, deficiencies,

deviations, defective material and equipment, and nonconformances are promptly

identified and corrected. Contrary to the above, between November 10 and

December 1, 2009, engineering personnel failed to adequately identify for correction a

condition adverse to quality. Specifically, the inspection of potential degradation

associated with the support welds and embedded wall plates for safety related seismic

pipe restraints for emergency core cooling piping was inadequate, in that, standing water

and corrosion product interference was not removed to enable an adequate inspection

and evaluation of the structural material. Adequate inspection and evaluation is

necessary, such that, the identified resolution addresses the causes and extent of

conditions. Because this finding is of very low safety significance and has been entered

into the licensees corrective action program as Nuclear Notification NN 200743417, this

violation is being treated as a noncited violation, consistent with Section VI.A of the NRC

Enforcement Policy: NCV 05000361/2009005-02, Failure to Adequately Identify

Problems in Corrective Action Program.

1R08 In-service Inspection Activities (71111.08)

.1 Inspection Activities Other Than Steam Generator Tube Inspection, Pressurized Water

Reactor Vessel Upper Head Penetration Inspections, and Boric Acid Corrosion Control

(71111.08-02.01)

a. Inspection Scope

The inspector reviewed two types of nondestructive examination activities and two welds

on the reactor coolant system pressure boundary. The inspector did not review

examinations with relevant indications that had been accepted by licensee personnel for

continued service because there were none.

The inspector directly observed the following nondestructive examinations:

SYSTEM WELD IDENTIFICATION EXAMINATION TYPE

Reactor Coolant 02-008-002 Ultrasonic Testing

System

Safety Injection 02-020-088 Penetrant Testing

System

The inspector reviewed records for the following nondestructive examinations:

SYSTEM WELD IDENTIFICATION EXAMINATION TYPE

Reactor Coolant 02-006-010 Ultrasonic Testing

System

High Pressure 02-068-950 Penetrant Testing

- 17 - Enclosure

SYSTEM WELD IDENTIFICATION EXAMINATION TYPE

Safety Injection

High Pressure 02-068-970 Penetrant Testing

Safety Injection

Low Pressure 02-071-1510 Penetrant Testing

Safety Injection

Low Pressure 02-071-1530 Penetrant Testing

Safety Injection

High Pressure 02-06-3640 Penetrant Testing

Safety Injection)

Low Pressure 02-071-1700 Penetrant Testing

Safety Injection

High Pressure 02-070-2710 Penetrant Testing

Safety Injection

High Pressure 02-068-990 Penetrant Testing

Safety Injection

High Pressure 02-070-2860 Penetrant Testing

Safety Injection

High Pressure 02-070-2370 Penetrant Testing

Safety Injection

Low Pressure 02-062-031-01 Penetrant Testing

Safety Injection

Low Pressure 02-072-137 Penetrant Testing

Safety Injection

Shutdown 02-075-042 Penetrant Testing

Cooling

During the review and observation of each examination, the inspector verified that

activities were performed in accordance with the ASME Code requirements and

applicable procedures. The inspector also verified that the qualifications of all

nondestructive examination technicians performing the inspections were current.

- 18 - Enclosure

The inspector observed performance of one ASME Code,Section XI, repair and

replacement weld and performed a record review of one additional weld. The weld that

was observed was:

SYSTEM IDENTIFICATION ACTIVITY

High Pressure Safety S21204MU021 Weld installation

Injection

The weld for which a record review was performed was:

SYSTEM IDENTIFICATION ACTIVITY

Chemical Volume Control 2TSH9205 Weld installation

System

The inspector verified, by review, that the welding procedure specifications and the

welders had been properly qualified in accordance with ASME Code,Section IX,

requirements. The inspector also verified, through observation and record review, that

essential variables for the welding process were identified, recorded in the procedure

qualification record, and formed the bases for qualification of the welding procedure

specifications. Specific documents reviewed during this inspection are listed in the

attachment.

These actions constitute completion of the requirements for Section 02.01.

b. Findings

No findings of significance were identified.

.2 Vessel Upper Head Penetration Inspection Activities (71111.08-02.02)

a. Inspection Scope

The inspector reviewed the results of licensee personnels volumetric inspection of

pressure-retaining components above the reactor pressure vessel head to verify that

there were no flaws in the welds associated with these penetrations. The inspector

observed data acquisition and/or analysis of five penetrations. The inspector verified

that the personnel performing the inspections were current in their certification as Level

II or Level III ultrasonic testing examiners. Specific documents reviewed during this

inspection are listed in the attachment.

These actions constitute completion of the requirements for Section 02.02.

b. Findings

No findings of significance were identified.

- 19 - Enclosure

.3 Boric Acid Corrosion Control Inspection Activities (71111.08-02.03)

a. Inspection Scope

The inspector evaluated the implementation of the licensees boric acid corrosion control

program for monitoring degradation of those systems that could be adversely affected by

boric acid corrosion. The inspector reviewed the documentation associated with the

licensees boric acid corrosion control walkdown as specified by Procedure SO23-XV-

85, Boric Acid Corrosion Control Program, Revision 4. The inspector also reviewed the

visual records of the components and equipment. The inspector verified that the visual

inspections emphasized locations where boric acid leaks could cause degradation of

safety-significant components. The inspector also verified that the engineering

evaluations for those components where boric acid was identified gave assurance that

the ASME Code wall thickness limits were properly maintained. The inspector confirmed

that the corrective actions performed for evidence of boric acid leaks were consistent

with requirements of the ASME Code. Specific documents reviewed during this

inspection are listed in the attachment.

These actions constitute completion of the requirements for Section 02.03.

b. Findings

No findings of significance were identified.

.4 Steam Generator Tube Inspection Activities (71111.08-02.04)

a. Inspection Scope

The licensee did not perform steam generator inspection activities this refueling outage.

Consequently, the inspector did not perform any inspections in this area.

These actions constitute completion of the requirements of Section 02.04.

b. Findings

No findings of significance were identified.

.5 Identification and Resolution of Problems (71111.08-02.05)

a. Inspection scope

The inspector reviewed nine condition reports which dealt with inservice inspection

activities and found the corrective actions were appropriate. The specific condition

reports reviewed are listed in the documents reviewed section. From this review the

inspector concluded that the licensee has an appropriate threshold for entering issues

into the corrective action program and has procedures that direct a root cause evaluation

when necessary. The licensee also has an effective program for applying industry

operating experience. Specific documents reviewed during this inspection are listed in

the attachment.

These actions constitute completion of the requirements of Section 02.05.

- 20 - Enclosure

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program (71111.11)

.1 Annual Inspection

The licensed operator requalification program involves two training cycles that are

conducted over a two year period. In the first cycle, the annual cycle, the operators are

administered an operating test consisting of job performance measures and simulator

scenarios. In the second part of the training cycle, the biennial cycle, operators are

administered an operating test and a comprehensive written examination.

a. Inspection Scope

The inspector conducted an in-office review of the annual requalification training

program operating test results for 2009. The licensee examined 87 operators

(41 reactor operators and 46 senior reactor operators) during this requalification cycle.

In addition, 15 operating crews were examined on the facility's simulator. Thirteen of the

operating crews passed the simulator scenarios and 84 operators passed the operating

tests.

b. Findings

No findings of significance were identified.

.2 Quarterly Inspection

a. Inspection Scope

On December 17, 2009, the inspectors observed a crew of licensed operators in the

plants simulator during licensed operator requalification training to verify that operator

performance was adequate, evaluators were identifying and documenting crew

performance problems, and training was being conducted in accordance with licensee

procedures. The inspectors evaluated the following areas:

  • Licensed operator performance
  • Crews clarity and formality of communications
  • Crews ability to take timely actions in the conservative direction
  • Crews prioritization, interpretation, and verification of annunciator alarms
  • Crews correct use and implementation of abnormal and emergency procedures
  • Control board manipulations
  • Oversight and direction from supervisors
  • Crews ability to identify and implement appropriate technical specification

actions and emergency plan actions and notifications

- 21 - Enclosure

The inspectors compared the crews performance in these areas to pre-established

operator action expectations and successful critical task completion requirements.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one quarterly licensed-operator requalification

program sample as defined in IP 71111.11.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk

significant systems:

  • November 17, 2009, Units 2 and 3, review of the noise spikes on emergency

diesel generator dc power bus

power supply problems

The inspectors reviewed events such as where ineffective equipment maintenance has

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

  • Implementing appropriate work practices
  • Identifying and addressing common cause failures
  • Characterizing system reliability issues for performance
  • Charging unavailability for performance
  • Trending key parameters for condition monitoring
  • Verifying appropriate performance criteria for structures, systems, and

components classified as having an adequate demonstration of performance

through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as

requiring the establishment of appropriate and adequate goals and corrective

actions for systems classified as not having adequate performance, as described

in 10 CFR 50.65(a)(1)

- 22 - Enclosure

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the corrective action program with the appropriate

significance characterization. Specific documents reviewed during this inspection are

listed in the attachment.

These activities constitute completion of three quarterly maintenance effectiveness

samples as defined in IP 71111.12-05.

b. Findings

The inspectors reviewed the events, and associated maintenance effectiveness that led

to the periods of emergency diesel generator inoperability described in Section 4OA3.1,

and identified two findings where the licensee failed to take adequate corrective actions

for conditions adverse to quality associated with the Unit 3 emergency diesel generators.

The inspectors determined that the underlying performance deficiencies that resulted in

the emergency diesel generator inoperability declarations were a failure to implement

corrective actions commensurate with the safety significance of the emergency diesel

generators.

1. Emergency Diesel Generator Train B

Introduction. The inspectors identified a Green noncited violation of 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, for the licensee's failure to take adequate

corrective actions for a condition adverse to quality associated with Unit 3 emergency

diesel generator train B.

Description. The inspectors reviewed the licensees prompt investigation into the

December 11, 2009, inadvertent grounding of a wire by a maintenance technician. The

inadvertent grounding blew the emergency diesel generator train B annunciator system

fuse. This investigation report was documented in Nuclear Notification NN 200704617

and indicated that a similar event caused the same fuse to blow in May 2009 during

scheduled maintenance on emergency diesel generator train B per Maintenance Order

MO 800295645. Following the event on December 11, engineering personnel

determined that the annunciator system must have had a preexisting ground in order for

the fuse to have been blown by either of these accidental groundings. The inspectors

questioned maintenance personnel familiar with the May 2009 event and identified that

the only corrective action taken at the time was to replace the blown fuse. The

inspectors concluded the licensee failed to take adequate corrective actions to perform

an evaluation of the failure, including the potential impact on operability and the need for

further corrective actions. These inadequate corrective actions enabled the pre-existing

ground condition to continue until it ultimately rendered the emergency diesel generator

train B inoperable on December 11, 2009.

Analysis. The failure to take adequate corrective actions for conditions adverse to

quality was a performance deficiency. The finding is greater than minor because the

failure to correct conditions adverse to quality for the emergency diesel generators is

associated with the equipment performance attribute of the Mitigating Systems

Cornerstone and affects the associated cornerstone objective to ensure the availability,

reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. Using the Manual Chapter 0609, Significance

Determination Process, Phase 1 Worksheets, the finding is determined to have very low

- 23 - Enclosure

safety significance because it did not represent an actual loss of safety function, and did

not screen as potentially risk significant due to a seismic, flooding, or severe weather

initiating event. This finding has a crosscutting aspect in the area of problem

identification and resolution associated with corrective action program since the licensee

failed to thoroughly evaluate problems such that the resolutions address the causes and

extent of conditions P.1(c).

Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,

Criterion XVI, Corrective Action, requires, in part, that measures shall be established to

assure that conditions adverse to quality, such as failures, malfunctions, deficiencies,

deviations, defective material and equipment, and nonconformances are promptly

identified and corrected. Contrary to the above, in May 2009, the licensee failed to take

adequate corrective actions for conditions adverse to quality associated with emergency

diesel generator train B. Specifically, corrective actions were inadequate following an

unexpected fuse failure in the emergency diesel generator train B annunciator system.

Because this finding was of very low safety significance and has been entered into the

licensees corrective action program as Nuclear Notification NN 200722170, this

violation is being treated as a noncited violation, consistent with Section VI.A of the NRC

Enforcement Policy: NCV 05000362/2009005-03, Failure to Correct Problems with

Emergency Diesel Generator Train B.

2. Emergency Diesel Generator Train A

Introduction. The inspectors identified a Green noncited violation of 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, for the licensee's failure to take adequate

corrective actions for a condition adverse to quality associated with Unit 3 emergency

diesel generator train A.

Description. On June 6, 2009, the emergency diesel generator train A was declared

inoperable after it failed to start during a monthly surveillance test. The cause was

determined to be voltage noise from the annunciator power supplies that incorrectly

closed contacts in the speed switch circuitry. As part of the immediate corrective actions,

the licensee modified the annunciator power supply circuit boards obtained from the

warehouse by replacing the capacitors with new capacitors, installed the power supplies

on June 13, 2009, and initiated an apparent cause evaluation.

Following the emergency diesel generator train A failure on December 12, the licensee

determined that the cause was the same cause as the failure on June 6, 2009. Further,

the licensees failure analysis concluded that both annunciator power supply circuit

boards (replaced on June 13, 2009), had configuration problems, in that, a capacitor was

in contact with an adjacent resistor. This configuration problem contributed to rapid

capacitor degradation as a result of the increased heat from the resistor, which ultimately

caused the emergency diesel generator failure to start on December 12. Emergency

diesel generator train A was successfully started, and completed a surveillance test on

November 23, 2009, then continued in a standby condition until the failure to start

occurred on December 12, 2009.

Analysis. The failure to take adequate corrective actions for conditions adverse to

quality was a performance deficiency. The finding is greater than minor because the

failure to correct conditions adverse to quality for the emergency diesel generators is

associated with the equipment performance attribute of the Mitigating Systems

Cornerstone and affects the associated cornerstone objective to ensure the availability,

- 24 - Enclosure

reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. Using the Manual Chapter 0609, Significance

Determination Process, Phase 1 Worksheets, the inspectors determined that this

finding represented an actual loss of safety function of an emergency diesel generator

train for greater than the technical specification allowed outage time. This required that

a Phase 2 estimation be completed. Because the Phase 2 analysis concluded that the

finding was potentially greater than green, a Phase 3 analysis was completed by a

regional senior reactor analyst. The San Onofre SPAR model indicated that the delta-

core damage frequency for emergency diesel generator train A being non-functional was

2.0E-6/yr. For an exposure time of 7 days, this resulted in an incremental core damage

frequency of 3.8E-8 for this finding, considering internal events only. The dominant

sequence was a station blackout sequence with failure of the diesels, failure to cross-tie

power from the other unit, failure to recover either onsite or offsite power, failure of

batteries at 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, and a failure to manually control the turbine-driven auxiliary

feedwater pump after battery depletion. The senior reactor analyst determined

qualitatively that the contribution of external events would not significantly add to this

result; therefore, the finding is determined to be of very low safety significance (Green).

This finding has a crosscutting aspect in the area of human performance associated with

resources because the licensee failed to provide adequate instructions to perform

activities affecting quality H.2(c).

Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,

Criterion XVI, Corrective Action, requires, in part, that measures shall be established to

assure that conditions adverse to quality, such as failures, malfunctions, deficiencies,

deviations, defective material and equipment, and nonconformances are promptly

identified and corrected. Contrary to the above, on June 13, 2009, the licensee failed to

take adequate corrective actions for conditions adverse to quality associated with the

emergency diesel generator train A. Specifically, the immediate corrective actions were

inadequately implemented when improperly configured annunciator power supplies were

installed in the emergency diesel generator train A annunciator system. Because this

finding was of very low safety significance and has been entered into the licensees

corrective action program as Nuclear Notification NN 200756001, this violation is being

treated as a noncited violation, consistent with Section VI.A of the NRC Enforcement

Policy: NCV 05000362/2009005-04, Failure to Correct Problems with Emergency Diesel

Generator Train A.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed licensee personnel's evaluation and management of plant risk

for the maintenance and emergent work activities affecting risk-significant and safety-

related equipment listed below to verify that the appropriate risk assessments were

performed prior to removing equipment for work:

  • October 6, 2009, Unit 2, reactor vessel head removal and storage
  • October 22-26, 2009, Unit 2, steam generator replacement impacts to operating

unit risk assessment

- 25 - Enclosure

temporary lift modifications to facilitate steam generator replacement

  • November 2-3, 2009, Units 2 and 3, emergent work activities associated with

atmospheric dump valves found with loose jam nut

  • November 12-24, 2009, Unit 2, fire damper engineering change package on

emergency cooling train A

The inspectors selected these activities based on potential risk significance relative to

the reactor safety cornerstones. As applicable for each activity, the inspectors verified

that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)

and that the assessments were accurate and complete. When licensee personnel

performed emergent work, the inspectors verified that the licensee personnel promptly

assessed and managed plant risk. The inspectors reviewed the scope of maintenance

work, discussed the results of the assessment with the licensee's probabilistic risk

analyst or shift technical advisor, and verified plant conditions were consistent with the

risk assessment. The inspectors also reviewed the technical specification requirements

and inspected portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of five maintenance risk assessments and

emergent work control inspection samples as defined by IP 71111.13-05.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors reviewed the following issues:

  • November 10, 2009, Units 2 and 3, styrofoam material in containment impact to

containment emergency sump

water storage tank to charging pump suction

water storage tank to charging pump suction

  • December 7, 2009, Unit 3, S32420MY719, flexible hose for the dc auxiliary turbo

pump P496 on emergency diesel generator train B

  • December 9, 2009, Units 2 and 3, operability impact of cracks identified on

mounting flanges for bushings associated with Class 1E 4.16 kV breakers

train B following annunciator power supply problems identified in train A

- 26 - Enclosure

  • December 22, 2009, Unit 3, boric acid deposits discovered on emergency core

cooling system train A suction piping

The inspectors selected these potential operability issues based on the risk-significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that technical specification operability was

properly justified and the subject component or system remained available such that no

unrecognized increase in risk occurred. The inspectors compared the operability and

design criteria in the appropriate sections of the technical specifications and Updated

Safety Analysis Report to the licensees evaluations, to determine whether the

components or systems were operable. Where compensatory measures were required

to maintain operability, the inspectors determined whether the measures in place would

function as intended and were properly controlled. The inspectors determined, where

appropriate, compliance with bounding limitations associated with the evaluations.

Additionally, the inspectors also reviewed a sampling of corrective action documents to

verify that the licensee was identifying and correcting any deficiencies associated with

operability evaluations. Specific documents reviewed during this inspection are listed in

the attachment.

These activities constitute completion of seven operability evaluations inspection

samples as defined in IP 71111.15-05.

b. Findings

1. Operability Determination Adequacy

Introduction. The inspectors identified three examples of a Green noncited violation of

10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures and Drawings, for

the failure of operations and engineering personnel to follow procedures and adequately

evaluate degraded conditions to support operability decision making.

Description. The first example is associated with issues discovered on October 27,

2009, when a fire was reported inside the Unit 2 containment at the 63 foot elevation.

The fire started while workers were using an acetylene torch to remove a vertical floor

support I-beam column, which was being removed to support steam generator

replacement activities. Hot slag from the torching activity burned into caulking around

the I-beam and ignited styrofoam material enclosed by the caulking. The styrofoam

spacer and caulking were used during original construction and are an integral part of

the containment floor design. The licensee documented this event in Nuclear

Notification NN 200643134.

The inspectors reviewed the event on October 28, 2009, and became aware that

engineering personnel were assigned tasks to determine the impact that styrofoam

material had on the containment emergency sump. Further, the inspectors were

informed the styrofoam material had not been analyzed as part of the licensee response

to NRC Generic Letter (GL) 2004-02, Potential Impact of Debris Blockage on

Emergency Sump Recirculation at Pressurized Water Reactors (PWRs).

On October 29, 2009, the inspectors questioned engineering personnel regarding the

status of the operability evaluation for Unit 3 and were told that there had been no task

assigned in the nuclear notification. Additional questions determined that engineering

personnel were only continuing their analysis of the impact that styrofoam material had

- 27 - Enclosure

on the containment emergency sump for Unit 2 as assigned by Nuclear Notification NN

200643134. Since this material was discovered in Unit 2, and was likely to exist in

Unit 3 as well, the inspectors asked if the condition was being evaluated for operability

since Unit 3 was in Mode 1. Specifically, the inspectors questioned whether an

evaluation of the specific Unit 3 conditions needed to be assessed through the

operability determination process as prescribed in Procedure SO123-XV-52,

Functionality Assessments and Operability Determinations, Revision 13. In addition,

the inspectors questioned whether an evaluation was necessary to review the impact of

the styrofoam on the fire loading analysis. Engineering personnel generated Nuclear

Notification NN 200645996, as a result of the inspectors questions, to perform an

operability determination for the Unit 3 emergency containment sump.

On November 3, 2009, the immediate operability and prompt operability determinations

were completed for Unit 3. The licensee determined that Unit 3 had a reasonable

expectation of operability based on three factors: 1) material discovered in the

containment was situated such that it was unlikely to become dislodged and free to

become entrained in a flow of water; 2) material was of low density and would float and

not likely to cause blockage at the emergency sump; and 3) material was not likely to be

affected by temperatures expected during any anticipated operational occurrences.

On November 4, 2009, fire protection engineers completed a functional assessment for

Unit 3, that evaluated styrofoam impact on the fire protection analysis. The evaluation

concluded that the styrofoam material was isolated from other combustibles and ignition

sources and therefore not an impact to safety related equipment inside containment.

The inspectors reviewed the operability determinations and functional assessments, and

concluded that they were adequate.

The second example was associated with equipment issues first identified on

November 17, 2009, when the licensee identified a lube oil leak from the Unit 3

emergency diesel generator train B. The leak was identified to be from the flexible hose

for the dc auxiliary turbo pump P496 and leaking at a rate of seven drops per minute.

The licensee initiated Nuclear Notification NN 200669151 to place the problems

associated with the leaking hose into the corrective action program. Subsequently, the

licensee, in accordance with Procedure SO123-XV-52, Functionality Assessments and

Operability Determinations, Revision 14, performed an immediate operability

determination to ensure that the leak would not challenge the minimum required lube oil

level stated in Technical Specification 3.8.3, Diesel Lube Oil, Fuel Oil and Starting Air,

and therefore meet the design basis seven day operation. The licensee determined,

using engineering judgment, that the diesel generator would still remain operable due to

the small leak rate. The licensee then performed a prompt operability determination,

based on the use of engineering judgment in the immediate operability determination,

which assumed that the leak rate would be proportional to the increase in pressure

during generator operation and reach a limit of ten drops per minute. The resulting

calculation determined that a total volume of oil that would be lost during the required

seven day operation would be only 1.33 gallons. This calculation did not include any

other unidentified leakage, which did not challenge the available ten percent margin

(16.46 gallons) built into the seven day oil consumption value for the diesel generator.

The licensee, due to the failure mechanism of the flex hose being unknown, commenced

periodic inspection of the leak location and leak rate estimations to ensure that further

degradation did not impact the 7 day mission time of the emergency diesel generator.

- 28 - Enclosure

The licensee did not identify an upper limit for leakage in which the 7 day mission time

would be challenged as part of the operability determination to provide guidance for the

engineers inspecting the leak.

On December 8, 2009, during operation of emergency diesel generator train B, a leak

was identified at a leak rate of 140 drops per minute from the degraded hose identified

on November 17, 2009, in Nuclear Notification NN 200669151. The licensee declared

emergency diesel generator train B inoperable following the identification of the lube oil

leak due to the increased leak rate and potential future degradation of the flexible hose.

The flexible hose was replaced as part of Maintenance Order NMO 800410821. The

previous operability determination assumed a leak rate of 10 drops per minute during

generator operation. Based on the observed leak rate, operations personnel determined

that the operability of the generator should be reassessed and initiated Nuclear

Notification NN 200695875. The licensee performed another prompt operability

determination using values obtained from Procedure SO23-3-3.23, Diesel Generator

Monthly and Semiannual Testing, Attachment 11, and assumptions used in the previous

evaluation and concluded that the amount of available oil to cover the seven day loss

due to the flex hose leakage was 18.74 gallons. The licensee determined that the 140

drop per minute leak rate from the flex hose corresponded to 18.64 gallons over the

design basis required seven day operation which resulted in a margin of .1 gallons. This

assumed that margin, 16.64 gallons, calculated into the total 181.1 gallons of oil required

for the completion of the seven day mission time would be used by the current active

leak and did not take into account additional leakage. During the December 8, 2009,

diesel run, the licensee identified another lube oil leak and replaced two additional

flexible hoses that showed evidence of seepage not accounted for in this assumption.

The licensee determined, based on these assumptions, that the emergency diesel

generator could meet the seven day mission time.

Procedure SO123-XV-52, defined a component operable if the structure, system, or

component is capable of performing the functions specified by its design, within the

required range of physical design conditions. Based on this, the inspectors questioned

the adequacy of using the assumption that the leak rate was proportional to the change

in pressure and that it did not take into account the changes in temperature

(~100 degree change) and viscosity of the lube oil during diesel generator operations. In

addition, the inspectors questioned the methodology used for determining the available

oil and converting the drop per minute leak rate to total lube oil loss due to the licensee

using a standard water drop to cubic centimeter ratio. The use of the standard ratio for

water did not account for any differences in viscosity and temperature between oil and

water. Following the inspectors questioning, the licensee conducted testing to

determine the actual drop rate to cubic centimeter per hour corresponding to the diesel

generator lube oil. The licensee determined that the more conservative value of ten

drops per cubic centimeter should be used to calculate the amount of lube oil lost during

the seven day operation instead of the initial value of twenty drops per cubic centimeter.

This change in conversion factors resulted in a calculated loss of approximately

37 gallons of lube oil over a seven day period of operation instead of the 18.64 gallons

previously assumed.

Following the inspectors questions about the methodology used in determining the

amount of oil available and lost due to leakage, the licensee recalculated the amount of

oil available above the minimum technical specification required level. The licensee

- 29 - Enclosure

determined that the diesel generator had a volume of approximately 42 gallons of oil

between the technical specification minimum level and the Full Run mark.

The third example occurred on December 19, 2009, following the identification of boric

acid deposits on the Unit 3 emergency core cooling system train A suction piping. The

boric acid deposits were observed on the welds attaching a lug to the pipe at support

S3-SI-001-H-030. Based on the deposits observed, the licensee determined that the

boric acid leakage was from a through wall flaw located underneath the lug. Because of

the leak location, the licensee was unable to characterize the flaw geometry. Instead,

engineering personnel assumed the flaw characteristics based on operating experience

and a determination that the critical crack length was greater than the size of the lug.

Since the flaw was determined to be within the boundary of the lug, the licensee

concluded that the flaw was less than the critical crack length. Based on the assumed

characterization of the flaw, the licensee applied the provisions of Code Case N-513-2,

Evaluation Criteria for Temporary Acceptance of Flaws in Moderate Energy Class 2 or 3

Piping, and determined that the emergency core cooling system train A suction piping

was operable.

On December, 22, 2009, the inspectors reviewed the operability determination

documented in Nuclear Notification NN 200714391 and Code Case N-513-2. The

inspectors reviewed Code Case N-513-2 and noted that it was only applicable when the

flaw geometry was characterized by volumetric inspection methods or by physical

measurements. The inspectors determined that the method used to characterize the

flaw to justify operability in the operability determination was not in accordance with the

code case, in that, the flaw geometry was only assumed and not characterized by

volumetric inspection methods or by physical measurements. Therefore, the inspectors

concluded that engineering and operations personnel inappropriately applied Code Case

N-513-2 to justify the operability of the emergency core cooling system train A.

The inspectors communicated their conclusion regarding the inadequate operability

determination to operations and engineering personnel. Since the operability

determination was inadequate, operations personnel declared the emergency core

cooling system train A suction piping, and refueling water storage tank inoperable and

entered applicable technical specifications and followed the requirements of the limiting

conditions for operability. Refueling water storage tank outlet isolation valve 3HV-9300

was closed to isolate the leak from the refueling water storage tank, which restored

operability of the tank. The emergency core cooling system train A remained inoperable.

The licensee removed the lugs necessary to complete the required inspections to

properly characterize the flaw geometry. Following flaw characterization, the licensee

appropriately applied Code Case N-513-2 to document an adequate basis for operability

of the piping in a revised operability determination, declared the emergency core cooling

system train A suction piping operable, and opened outlet isolation valve 3HV-9300 to

return the system to service.

Analysis. The failure to perform an adequate operability determination was a

performance deficiency. The finding is greater than minor because the failure to perform

timely and adequate evaluations of degraded, nonconforming, and unanalyzed

conditions for operability, if left uncorrected, would have the potential to lead to a more

significant safety concern. The finding is associated with the equipment performance

attribute of the Mitigating Systems Cornerstone and affects the associated cornerstone

- 30 - Enclosure

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Using the Manual Chapter 0609,

Significance Determination Process, Phase 1 Worksheets, the finding is determined to

have very low safety significance because the finding did not result in a loss of safety

function for greater than the technical specification allowed outage time, and did not

screen as potentially risk significant due to a seismic, flooding, or severe weather

initiating event. This finding has a crosscutting aspect in the area of problem

identification and resolution associated with corrective action program because

operations and engineering personnel failed to thoroughly evaluate problems such that

the resolutions addressed the cause and extent of condition. This includes properly

classifying, prioritizing, and evaluating for operability conditions adverse to quality

P.1(c).

Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,

Criterion V, Instructions, Procedures and Drawings, requires that activities affecting

quality shall be prescribed by instructions, procedures, or drawings and shall be

accomplished in accordance with those instructions, procedures, and drawings. The

assessment of operability of safety related equipment needed to mitigate accidents was

an activity affecting quality and was implemented by Procedure SO123-XV-52,

Functionality Assessments and Operability Determinations. Procedure SO123-XV-52,

Step 1.0, stated that the objective of the procedure was to provide guidelines and

instructions for evaluating the operability of a structure, system, or component when a

degraded, nonconforming, or unanalyzed condition was identified.

Contrary to the above, on October 29, 2009, engineering personnel failed to follow

Procedure SO123-XV-52, Revision 13, to adequately evaluate the operability of an

identified nonconforming and unanalyzed condition. Specifically, engineering personnel

failed to adequately evaluate the operability of the Unit 3 containment emergency sump

when an unanalyzed styrofoam material was identified, which had not been previously

analyzed for impact to the containment emergency sump.

Contrary to the above, on November 17 and December 8, 2009, operations and

engineering personnel failed to follow Procedure SO123-XV-52, Revision 14, to

adequately evaluate the operability of the Unit 3 emergency diesel generator train B.

Specifically, operations and engineering personnel failed to adequately evaluate the

operability of emergency diesel generator train B when a lube oil leak was identified on a

flexible hose for the dc auxiliary turbo pump.

Contrary to the above, on December 19, 2009, operations and engineering personnel

failed to follow Procedure SO123-XV-52, Revision 14, to adequately evaluate the

operability of the Unit 3 emergency core cooling system train A. Specifically, operations

and engineering personnel inappropriately applied Code Case N-513-2 to justify the

operability of the emergency core cooling system train A, in that, the flaw geometry was

only assumed and not characterized by volumetric inspection methods or by physical

measurements.

Because the finding is of very low safety significance and has been entered into the

licensees corrective action program as Nuclear Notifications NNs 200673198,

200699833, and 200718673, this violation is being treated as a noncited violation,

consistent with Section VI.A of the Enforcement Policy: NCV 05000362/2009005-05,

Failure to Follow the Operability Determination Process.

- 31 - Enclosure

2. Compensatory Measures

Introduction. The inspectors identified a Green noncited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures and Drawings, for the failure of

operations personnel to follow procedures and adequately implement identified

compensatory measures used to substitute manual operator actions for automatic

actions to perform a required function.

Description. On November 25, 2009, through wall leaks were identified on piping from

the refueling water storage tank to charging pump suction on Units 2 and 3. Unit 3

entered a one hour shutdown action per Technical Specification 3.5.4, Condition B, for

an inoperable refueling water storage tank. Unit 3 exited the one hour action statement

when block valves MU067 and MU054 were closed to isolate the leaks from the

refueling water storage tank. Unit 2 was defueled when the through wall leaks were

discovered. The Unit 2 shutdown defense in depth strategy credited the refueling water

storage tank to charging pump suction line as a makeup source to control spent fuel pool

inventory. Similar to actions taken in Unit 3, operations personnel in Unit 2 shut block

valve MU067 to isolate a leak from the Unit 2 refueling water storage tank.

The refueling water storage tank to charging pump suction piping for Units 2 and 3 were

preliminarily determined to be operable through application of Code Case N-513-2,

Evaluation Criteria for Temporary Acceptance of Flaws in Moderate Energy Class 2 or 3

Piping. Subsequently, procedure modification permits were prepared per Procedure

SO123-0-A3, Procedure Use, Revision 8, for Unit 2 on November 25, and for Unit 3 on

November 28, to open the block valves to support operability of the functions provided

by the refueling water storage tank to charging pump suction piping. Specifically, Unit 2

initiated a procedure modification permit to modify Procedure SO23-3-2.11.1, SFP

Level Change and Purification Crosstie Operations, Revision 14, to open block valve

MU067 and maintain the ability to makeup to the spent fuel pool using the refueling

water storage tank and spent fuel pool pump. Unit 3 initiated a procedure modification

permit to modify the abnormal operating instruction Procedure SO23-13-2, Shutdown

from Outside the Control Room, Revision 12, to open block valves MU067 and MU054

to maintain the boron flow path provided by the refueling water storage tank to charging

pump suction pipe. The intention of the procedure modification permits was to replace

the automatic opening of valves with the local manual opening of block valves.

On December 2, 2009, the inspectors reviewed the actions taken by operation personnel

in response to the identification of the through wall leaks identified on Units 2 and 3. The

inspectors noted that block valves remained closed on Units 2 and 3 and questioned

operations personnel whether the refueling water storage tank to charging pump suction

lines were considered operable. Operations personnel presented the procedure

modification permits to the inspectors and explained that the procedure modifications

were being used to support operability of the functions provided by the piping. The

inspectors reviewed the procedure modification permit and noted that the actions were

described as maintenance activities rather than compensatory measures used to

substitute manual operator actions for automatic actions to perform a required function.

Consequently, the required 10 CFR 50.59 screening was not performed. Further, the

inspectors questioned whether the requirements of Procedure SO123-XV-52,

Functionality Assessments and Operability Determinations, Revision 14,

Attachment 10, were followed for the use of compensatory measures to support

operability/functionality. The inspectors reviewed Procedure SO123-XV-52,

- 32 - Enclosure

Attachment 10, and observed that Step 1.8, stated, in part, that A compensatory

measure is NOT a maintenance activity, which was contrary to the descriptions on the

procedure modification permits.

In conclusion, the inspectors determined that operations personnel did not follow the

requirements of Procedure SO123-XV-52, Attachment 10, to perform a screening per

10 CFR 50.59 and review additional considerations necessary for the procedure

modification permits that were implemented as compensatory measures. Operations

personnel initiated Nuclear Notification NN 200689450 to document the failure to follow

Procedure SO123-XV-52, and actions were taken to comply with the requirements.

Analysis. The failure to follow procedures and adequately implement identified

compensatory measures to support operability/functionality was a performance

deficiency. The finding is greater than minor because the inadequate implementation of

compensatory measures, if left uncorrected, would have the potential to lead to a more

significant safety concern. The finding is associated with the procedure quality attribute

of the Mitigating Systems Cornerstone and affects the associated cornerstone objective

to ensure the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. Using the Manual Chapter 0609,

Significance Determination Process, Phase 1 Worksheets, the finding is determined to

have very low safety significance because the finding did not result in an actual loss of

safety function, and did not screen as potentially risk significant due to a seismic,

flooding, or severe weather initiating event. This finding has a crosscutting aspect in the

area of human performance associated with decision making because operations

personnel failed to make decisions using a systematic process, especially when faced

with uncertain or unexpected plant conditions, to ensure safety is maintained H.1(a).

Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,

Criterion V, Instructions, Procedures and Drawings, requires that activities affecting

quality shall be prescribed by instructions, procedures, or drawings and shall be

accomplished in accordance with those instructions, procedures, and drawings. The use

of compensatory measures to substitute manual operator actions for automatic actions

to perform a required function needed to mitigate accidents was an activity affecting

quality and was implemented by Procedure SO123-XV-52, Functionality Assessments

and Operability Determinations, Revision 14, Attachment 10, Guidance for Use of

Compensatory Measures to Support Operability/Functionality. Contrary to the above,

on November 25 and November 28, 2009, operations personnel failed to follow

Procedure SO123-XV-52. Specifically, operations personnel did not follow requirements

to establish a compensatory measure to substitute manual operator actions for

automatic actions to support the operability of the functions provided by the refueling

water storage tank to charging pump suction piping. Because the finding is of very low

safety significance and has been entered into the licensees corrective action program

as Nuclear Notification NN 200689450, this violation is being treated as a noncited

violation, consistent with Section VI.A of the NRC Enforcement Policy: NCV 05000361;05000362/2009005-06, Failure to Adequately Implement Compensatory Measures to

Maintain Equipment Operable.

- 33 - Enclosure

1R18 Plant Modifications (71111.18)

.1 Temporary Modifications

a. Inspection Scope

To verify that the safety functions of important safety systems were not degraded, the

inspectors reviewed the temporary modification identified as installation and testing of

containment jib crane and heavy lift devices associated with Unit 2 steam generator

replacement activities.

The inspectors reviewed the temporary modifications and the associated safety-

evaluation screening against the system design bases documentation, including the

Updated Final Safety Analysis Report and the technical specifications, and verified that

the modification did not adversely affect the system operability/availability. The

inspectors also verified that the installation and restoration were consistent with the

modification documents and that configuration control was adequate. Additionally, the

inspectors verified that the temporary modification was identified on control room

drawings, appropriate tags were placed on the affected equipment, and licensee

personnel evaluated the combined effects on mitigating systems and the integrity of

radiological barriers.

These activities constitute completion of one sample for temporary plant modifications as

defined in Inspection Procedure 71111.18-05.

b. Findings

No findings of significance were identified.

.2 Permanent Modifications

a. Inspection Scope

The inspectors reviewed key parameters associated with energy needs, materials,

replacement components, timing, heat removal, control signals, equipment protection

from hazards, operations, flow paths, pressure boundary, ventilation boundary,

structural, process medium properties, licensing basis, and failure modes for the

permanent modification associated with Unit 2 replacement steam generator skirt bolt

hole enlargement and stud deletion.

The inspectors verified that modification preparation, staging, and implementation did not

impair emergency/abnormal operating procedure actions, key safety functions, or

operator response to loss of key safety functions; postmodification testing will maintain

the plant in a safe configuration during testing by verifying that unintended system

interactions will not occur; systems, structures and components performance

characteristics still meet the design basis; the modification design assumptions were

appropriate; the modification test acceptance criteria will be met; and licensee personnel

identified and implemented appropriate corrective actions associated with permanent

plant modifications. Specific documents reviewed during this inspection are listed in the

attachment.

- 34 - Enclosure

These activities constitute completion of one sample for permanent plant modifications

as defined in Inspection Procedure 71111.18-05.

b. Findings

No findings of significance were identified.

1R19 Postmaintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed the following postmaintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

  • November 5, 2009, Unit 3, pressurizer level control valve 3LV0110B flow limiter

adjustment

  • November 9, 2009, Unit 2, spent fuel pool cooling pump 2P009 restoration to

normal power supply

  • November 26, 2009, Unit 3, return to service testing for pressurizer pressure

instrument channel A

  • December 4, 2009, Unit 2, 4.16 kV class 1E bus 2A06
  • December 8, 2009, Unit 3, flexible hose for the dc auxiliary turbo pump for

emergency diesel generator train B

  • December 23, 2009, Unit 2, emergency cooling unit 2ME255 train A following

thermal overload replacement

The inspectors selected these activities based upon the structure, system, or

component's ability to affect risk. The inspectors evaluated these activities for the

following (as applicable):

  • The effect of testing on the plant had been adequately addressed; testing was

adequate for the maintenance performed

  • Acceptance criteria were clear and demonstrated operational readiness; test

instrumentation was appropriate

The inspectors evaluated the activities against the technical specifications, the Updated

Final Safety Analysis Report, 10 CFR Part 50 requirements, licensee procedures, and

various NRC generic communications to ensure that the test results adequately ensured

that the equipment met the licensing basis and design requirements. In addition, the

inspectors reviewed corrective action documents associated with postmaintenance tests

to determine whether the licensee was identifying problems and entering them in the

corrective action program and that the problems were being corrected commensurate

with their importance to safety. Specific documents reviewed during this inspection are

listed in the attachment.

- 35 - Enclosure

These activities constitute completion of six postmaintenance testing inspection samples

as defined in IP 71111.19-05.

b. Findings

No findings of significance were identified.

1R20 Refueling and Other Outage Activities (71111.20)

a. Inspection Scope

The inspectors reviewed the outage safety plan and contingency plans for the Unit 2

refueling outage (U2C16) and steam generator replacement that commenced on

September 27, 2009, to confirm that licensee personnel had appropriately considered

risk, industry experience, and previous site-specific problems in developing and

implementing a plan that assured maintenance of defense-in-depth. NRC Inspection

Report 05000361/2009007 will document inspections and findings associated with

steam generator replacement. During the refueling outage, the inspectors observed

portions of the shutdown and cooldown processes and monitored licensee controls over

the outage activities listed below.

  • Configuration management, including maintenance of defense-in-depth, is

commensurate with the outage safety plan for key safety functions and

compliance with the applicable technical specifications when taking equipment

out of service.

  • Clearance activities, including confirmation that tags were properly hung and

equipment appropriately configured to safely support the work or testing.

  • Installation and configuration of reactor coolant pressure, level, and temperature

instruments to provide accurate indication, accounting for instrument error.

  • Status and configuration of electrical systems to ensure that technical

specifications and outage safety-plan requirements were met, and controls over

switchyard activities.

  • Verification that outage work was not impacting the ability of the operators to

operate the spent fuel pool cooling system.

alternative means for inventory addition, and controls to prevent inventory loss.

  • Controls over activities that could affect reactivity.

specifications.

  • Refueling activities, including fuel handling and sipping to detect fuel assembly

leakage.

- 36 - Enclosure

  • Licensee identification and resolution of problems related to refueling outage

activities.

Specific documents reviewed during this inspection are listed in the attachment.

Refueling outage U2C16 was still in progress at the end of this inspection period.

Consequently, these activities constitute only partial completion of one refueling outage

and other outage inspection sample as defined in IP 71111.20-05.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the Updated Final Safety Analysis Report, procedure

requirements, and technical specifications to ensure that the five surveillance activities

listed below demonstrated that the systems, structures, and/or components tested were

capable of performing their intended safety functions. The inspectors either witnessed or

reviewed test data to verify that the significant surveillance test attributes were adequate

to address the following:

  • Preconditioning
  • Evaluation of testing impact on the plant
  • Acceptance criteria
  • Test equipment
  • Procedures
  • Jumper/lifted lead controls
  • Test data
  • Testing frequency and method demonstrated technical specification operability
  • Test equipment removal
  • Restoration of plant systems
  • Fulfillment of ASME Code requirements
  • Updating of performance indicator data
  • Engineering evaluations, root causes, and bases for returning tested systems,

structures, and components not meeting the test acceptance criteria were correct

  • Reference setting data

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The inspectors also verified that licensee personnel identified and implemented any

needed corrective actions associated with the surveillance testing.

comprehensive full flow surveillance test

  • October 8, 2009, Unit 2, local leak rate test of penetration 21, service air to

containment, to include the installed blind flanges

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of five surveillance testing inspection samples as

defined in IP 71111.22-05.

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP1 Exercise Evaluation (71114.01)

a. Inspection Scope

The inspectors reviewed the objectives and scenario for the 2009 biennial emergency

plan exercise to determine if the exercise would acceptably test major elements of the

emergency plan. The scenario simulated a spill of contaminated material within the

plant, a reactor pressure transient caused by a failed reactor coolant pump causing

damage to reactor fuel cladding, a steam line break in containment, a fire on licensee

property leading to a loss of offsite power for both reactor units, a diesel generator failure

that resulted in station blackout conditions for Unit 2, and a radiological release to the

environment via a steam generator tube leak, to demonstrate licensee personnels

capability to implement their emergency plan.

The inspectors evaluated exercise performance by focusing on the risk-significant

activities of event classification, offsite notification, recognition of offsite dose

consequences, and development of protective action recommendations, in the Control

Room Simulator and the following dedicated emergency response facilities:

  • Operations Support Center
  • Emergency Operations Facility

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The inspectors also assessed recognition of, and response to, abnormal and emergency

plant conditions, the transfer of decision making authority and emergency function

responsibilities between facilities, onsite and offsite communications, protection of

emergency workers, emergency repair evaluation and capability, and the overall

implementation of the emergency plan to protect public health and safety and the

environment. The inspectors reviewed the current revision of the facility emergency

plan, emergency plan implementing procedures associated with operation of the

licensees emergency response facilities, procedures for the performance of associated

emergency functions, and other documents as listed in the attachment to this report.

The inspectors compared the observed exercise performance with the requirements in

the facility emergency plan, 10 CFR 50.47(b), 10 CFR Part 50, Appendix E, and with the

guidance in the emergency plan implementing procedures and other federal guidance.

The inspectors attended the post-exercise critiques in each emergency response facility

to evaluate the initial licensee self-assessment of exercise performance. The inspectors

also attended a subsequent formal presentation of critique items to plant management.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one sample as defined in Inspection

Procedure 71114.01-05.

b. Findings

No findings of significance were identified.

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

a. Inspection Scope

The inspector performed in-office and on-site reviews of licensee changes to the San

Onofre Nuclear Generating Station Emergency Plan, Revisions 25 and 26, both received

June 23, 2009, emergency plan implementing procedure SO123-VIII-1, Recognition and

Classification of Emergencies, Revision 28, submitted August 28, 2009, and San Onofre

Nuclear Generating Station Emergency Plan, Revision 27, implemented September 9,

2009. These revisions:

  • Revised the licensees goal for staffing their emergency response facilities from

sixty minutes to ninety minutes;

to the Emergency Operations Facility;

  • Moved the Effluent Engineer and Administrative Leader positions from the

Technical Support Center to the Emergency Operations Facility (EOF);

  • Deleted the EOF Offsite Dose Assessment Liaison, and Medical Team positions

from the emergency response organization;

  • Deleted the Emergency Classification and Event Code Chart;

- 39 - Enclosure

  • Combined the positions of Emergency News Center Technical Liaison and

Emergency News Center Communications Liaison;

  • Clarified that Corporate Emergency Director is responsible for evacuating the

site, and the Station Emergency Director is responsible for conducting site

assembly and accountability;

  • Added licensed Reactor Operators to the personnel qualified to fill the Control

Room Emergency Notification System Communicator positions;

  • Added offsite monitoring teams (four technicians) to the minimum staff positions

required to be present to activate the Emergency Operations Facility;

  • Added the EOF Health Physics Communicator position to the emergency

response organization;

  • Added the Electrical Technician, Instrument and Control Technician, and five

Health Physics Technicians as required minimum staff positions to activate the

Operations Support Center;

  • Added description of the duties of the environmental monitoring teams;
  • Added several emergency response organization positions to Table 5-2,

Emergency Response Organization Duties;

  • Added Table 5-5, Emergency Response Organization Minimum Staff Positions;
  • Added directions for handling an inoperable plant vent stack radiation monitor to

emergency action level A1;

  • Added clarifying information to emergency action level B1 to identify that steam

generator and chemical volume and control system leakage are included in the

25 gpm identified leakage criteria;

  • Added clarifying information to emergency action level B3 to identify the

alternative release paths to the environment to be considered, and specify that

the calculation of release time begins when charging pump capacity is exceeded;

  • Added clarifying information to emergency action level D3 to identify that the

reactor has failed to manually trip when any combination of Manual Reactor Trip

Pushbuttons are unsuccessful in tripping the reactor (initiating condition 5), and

that a loss of normal or auxiliary feedwater applies to uncontrolled reactor coolant

system temperature (initiating condition 7);

  • Updated emergency response organization position titles;
  • Updated titles of offsite emergency response organizations; and,
  • Made minor editorial corrections.

The NRC approved the licensees proposal to change their timeliness goal for staffing

their emergency response facilities from sixty minutes to ninety minutes in a Safety

- 40 - Enclosure

Analysis Report dated November 28, 2008 (Agency Document and Management

System Accession Numbers ML071700672, ML082740060, and ML0832306080).

These revisions were compared to their previous revision, to the criteria of NUREG-

0654, Criteria for Preparation and Evaluation of Radiological Emergency Response

Plans and Preparedness in Support of Nuclear Power Plants, Revision 1, and to the

standards in 10 CFR 50.47(b) to determine if the revision adequately implemented the

requirements of 10 CFR 50.54(q). These reviews were not documented in safety

evaluation reports and did not constitute approvals of licensee-generated changes;

therefore, these revisions are subject to future inspection. The specific documents

reviewed during this inspection are listed in the attachment.

The inspector also performed an in-office review of the licensees emergency plan

implementing procedure SO123-VIII-1, Recognition and Classification of Emergencies,

Revision 29, submitted October 14, 2009. This revision added a note describing the

validation of a fire alarm to Emergency Action Level E1-1, A Fire which is not declared

extinguished by the Fire Incident Commander within 15 minutes of Control Room

Notification or verification of a Control Room alarm.

This revision was compared to its previous revision, to the criteria of NUREG-0654,

Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and

Preparedness in Support of Nuclear Power Plants, Revision 1, and to the standards in

10 CFR 50.47(b) to determine if the revision adequately implemented the requirements

of 10 CFR 50.54(q). This review was not documented in a safety evaluation report and

did not constitute approval of licensee-generated changes; therefore, this revision is

subject to future inspection.

These activities constitute completion of five samples as defined in Inspection

Procedure 71114.04-05.

b. Findings

No findings of significance were identified.

1EP6 Drill Evaluation (71114.06)

Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors evaluated the conduct of a routine licensee emergency drill on November

18, 2009, to identify any weaknesses and deficiencies in classification, notification, and

protective action recommendation development activities. The inspectors observed

emergency preparedness mini drills to determine whether the event classification,

notifications, and protective action recommendations were performed in accordance with

procedures. The inspectors also attended the licensee drill critique to compare any

inspector-observed weakness with those identified by the licensee staff in order to

evaluate the critique and to verify whether the licensee staff was properly identifying

weaknesses and entering them into the corrective action program. As part of the

inspection, the inspectors reviewed the drill scenarios and other documents listed in the

attachment.

- 41 - Enclosure

These activities constitute completion of one sample as defined in IP 71114.06-05.

b. Findings

No findings of significance were identified.

2. RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

a. Inspection Scope

This area was inspected to assess licensee personnels performance in implementing

physical and administrative controls for airborne radioactivity areas, radiation areas, high

radiation areas, and worker adherence to these controls. The inspectors used the

requirements in 10 CFR Part 20, the technical specifications, and the licensees

procedures required by technical specifications as criteria for determining compliance.

During the inspection, the inspectors interviewed the radiation protection manager,

radiation protection supervisors, and radiation workers. The inspectors performed

independent radiation dose rate measurements and reviewed the following items:

  • Performance indicator events and associated documentation packages reported

by the licensee in the Occupational Radiation Safety Cornerstone

  • Controls (surveys, posting, and barricades) of radiation, high radiation, or

airborne radioactivity areas

  • Radiation work permits, procedures, engineering controls, and air sampler

locations

  • Conformity of electronic personal dosimeter alarm set points with survey

indications and plant policy; workers knowledge of required actions when their

electronic personnel dosimeter noticeably malfunctions or alarms

areas

  • Physical and programmatic controls for highly activated or contaminated

materials (non-fuel) stored within spent fuel and other storage pools

  • Self-assessments, audits, licensee event reports, and special reports related to

the access control program since the last inspection

  • Corrective action documents related to access controls
  • Licensee actions in cases of repetitive deficiencies or significant individual

deficiencies

  • Radiation work permit briefings and worker instructions

- 42 - Enclosure

  • Adequacy of radiological controls, such as required surveys, radiation protection

job coverage, and contamination control during job performance

  • Dosimetry placement in high radiation work areas with significant dose rate

gradients

and very high radiation areas

  • Controls for special areas that have the potential to become very high radiation

areas during certain plant operations

  • Posting and locking of entrances to all accessible high dose rate - high radiation

areas and very high radiation areas

  • Radiation worker and radiation protection technician performance with respect to

radiation protection work requirements

Either because the conditions did not exist or an event had not occurred, no

opportunities were available to review the following item:

  • Adequacy of the licensees internal dose assessment for any actual internal

exposure greater than 50 millirem committed effective dose equivalent

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of 21 of the required 21 samples as defined in

Inspection Procedure 71121.01-05.

b. Findings

No findings of significance were identified.

2OS2 ALARA Planning and Controls (71121.02)

a. Inspection Scope

The inspectors assessed licensee personnels performance with respect to maintaining

individual and collective radiation exposures as low as is reasonably achievable. The

inspectors used the requirements in 10 CFR Part 20 and the licensees procedures

required by technical specifications as criteria for determining compliance. The

inspectors interviewed licensee personnel and reviewed the following:

  • Dose rate reduction activities in work planning
  • Workers use of the low dose waiting areas
  • Records detailing the historical trends and current status of tracked plant source

terms and contingency plans for expected changes in the source term due to

changes in plant fuel performance issues or changes in plant primary chemistry

- 43 - Enclosure

  • Radiation worker and radiation protection technician performance during work

activities in radiation areas, airborne radioactivity areas, or high radiation areas

  • Declared pregnant workers during the current assessment period, monitoring

controls, and the exposure results

  • Self-assessments, audits, and special reports related to the ALARA program

since the last inspection

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of 4 of the required 15 samples and 2 of the

optional samples as defined in Inspection Procedure 71121.02-05.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

.1 Data Submission Issue

a. Inspection Scope

The inspectors performed a review of the data submitted by the licensee for the

Third Quarter 2009 performance indicators for any obvious inconsistencies prior to its

public release in accordance with Inspection Manual Chapter 0608, Performance

Indicator Program.

This review was performed as part of the inspectors normal plant status activities and,

as such, did not constitute a separate inspection sample.

b. Findings

No findings of significance were identified.

.2 Safety System Functional Failures (MS05)

a. Inspection Scope

The inspectors sampled licensee submittals for the safety system functional failures

performance indicators for Units 2 and 3 for the period from the 4th quarter 2008 through

the 3rd quarter 2009. To determine the accuracy of the performance indicator data

reported during those periods, the inspectors used definitions and guidance contained in

NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 5, and NUREG-1022, Event Reporting Guidelines 10 CFR 50.72 and 50.73."

The inspectors reviewed the licensees operator narrative logs, operability assessments,

maintenance rule records, maintenance work orders, issue reports, event reports, and

NRC integrated inspection reports for the period of October 2008 through September

2009, to validate the accuracy of the submittals. The inspectors also reviewed the

licensees issue report database to determine if any problems had been identified with

- 44 - Enclosure

the performance indicator data collected or transmitted for this indicator and none were

identified. Specific documents reviewed are described in the attachment to this report.

These activities constitute completion of two safety system functional failures sample as

defined in Inspection Procedure 71151-05.

b. Findings

No findings of significance were identified.

.3 Reactor Coolant System Specific Activity (BI01)

a. Inspection Scope

The inspectors sampled licensee submittals for the reactor coolant system specific

activity performance indicator for Units 2 and 3 for the period from the 4th quarter 2008

through the 3rd quarter 2009. To determine the accuracy of the performance indicator

data reported during those periods, the inspectors used definitions and guidance

contained in NEI Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 5. The inspectors reviewed the licensees reactor coolant system

chemistry samples, technical specification requirements, issue reports, event reports,

and NRC integrated inspection reports for the period of October 2008 through

September 2009 to validate the accuracy of the submittals. The inspectors also

reviewed the licensees issue report database to determine if any problems had been

identified with the performance indicator data collected or transmitted for this indicator

and none were identified. In addition to record reviews, the inspectors observed a

chemistry technician obtain and analyze a reactor coolant system sample. Specific

documents reviewed are described in the attachment to this report.

These activities constitute completion of two reactor coolant system specific activity

sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings of significance were identified.

.4 Occupational Exposure Control Effectiveness

a. Inspection Scope

The inspectors sampled licensee submittals for the Occupational Radiological

Occurrences performance indicator for the period from the 2nd quarter 2009 through the

3rd quarter 2009. To determine the accuracy of the performance indicator data reported

during those periods, performance indicator definitions and guidance contained in NEI

Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5,

was used. The inspectors reviewed the licensees assessment of the performance

indicator for occupational radiation safety to determine if indicator related data was

adequately assessed and reported. To assess the adequacy of the licensees

performance indicator data collection and analyses, the inspectors discussed with

radiation protection staff, the scope and breadth of its data review, and the results of

those reviews. The inspectors independently reviewed electronic dosimetry dose rate

and accumulated dose alarm and dose reports and the dose assignments for any

- 45 - Enclosure

intakes that occurred during the time period reviewed to determine if there were

potentially unrecognized occurrences. The inspectors also conducted walkdowns of

numerous locked high and very high radiation area entrances to determine the adequacy

of the controls in place for these areas.

These activities constitute completion of the occupational radiological occurrences

sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings of significance were identified.

.5 Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual

Radiological Effluent Occurrences

a. Inspection Scope

The inspectors sampled licensee submittals for the Radiological Effluent Technical

Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences

performance indicator for the period from the 2nd quarter 2009 through the 3rd quarter

2009. To determine the accuracy of the performance indicator data reported during

those periods, performance indicator definitions and guidance contained in NEI

Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5,

was used. The inspectors reviewed the licensees issue report database and selected

individual reports generated since this indicator was last reviewed to identify any

potential occurrences such as unmonitored, uncontrolled, or improperly calculated

effluent releases that may have impacted offsite dose.

These activities constitute completion of the radiological effluent technical

specifications/offsite dose calculation manual radiological effluent occurrences sample

as defined in Inspection Procedure 71151-05.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical

Protection

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees

corrective action program at an appropriate threshold, that adequate attention was being

given to timely corrective actions, and that adverse trends were identified and

addressed. The inspectors reviewed attributes that included: the complete and accurate

identification of the problem; the timely correction, commensurate with the safety

- 46 - Enclosure

significance; the evaluation and disposition of performance issues, generic implications,

common causes, contributing factors, root causes, extent of condition reviews, and

previous occurrences reviews; and the classification, prioritization, focus, and timeliness

of corrective actions. Minor issues entered into the licensees corrective action program

because of the inspectors observations are included in the attached list of documents

reviewed.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure, they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b. Findings

No findings of significance were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees corrective action program. The inspectors

accomplished this through review of the stations daily corrective action documents.

The inspectors performed these daily reviews as part of their daily plant status

monitoring activities and, as such, did not constitute any separate inspection samples.

b. Findings

No findings of significance were identified.

.3 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensees corrective action program and

associated documents to identify trends that could indicate the existence of a more

significant safety issue. The inspectors focused their review on repetitive equipment

issues, but also considered the results of daily corrective action item screening

discussed in Section 4OA2.2, above, licensee trending efforts, and licensee human

performance results. The inspectors nominally considered the six month period of July

2009 through December 2009, although some examples expanded beyond those dates

where the scope of the trend warranted.

The inspectors also included issues documented outside the normal corrective action

program in major equipment problem lists, repetitive and/or rework maintenance lists,

departmental problem/challenges lists, system health reports, quality assurance

audit/surveillance reports, self-assessment reports, and Maintenance Rule assessments.

The inspectors compared and contrasted their results with the results contained in the

licensees corrective action program trending reports. Corrective actions associated with

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a sample of the issues identified in the licensees trending reports were reviewed for

adequacy.

These activities constitute completion of one semi-annual trend inspection sample as

defined in IP 71152-05.

b. Observations and Findings

Based on the inspectors observation of an inadequate log keeping trend, Nuclear

Notification NN 200614441 was initiated for operations personnel to perform a three

month log review to determine whether entries satisfied the requirements of Procedure

SO123-0-A1, Conduct of Operations, Revision 26.

The assessment confirmed the inspectors observations and concluded that operator

logs were inconsistent and did not meet procedure intent for context, clarity, and closure.

Although some entries included the elements as described in Procedure SO123-0-A1 for

operable and inoperable, they were inconsistent with the standard. Consequently, it

became difficult to determine the logic used for determining operability and inoperability.

As a result of the assessment, Nuclear Notification NN 200685073 was initiated to

review the issues through an apparent cause evaluation.

.4 Selected Issue Follow-up Inspection

a. Inspection Scope

During a review of items entered in the licensees corrective action program, the

inspectors recognized a corrective action item documenting the issue listed below. The

inspectors considered the following during the review of the licensees actions: (1)

complete and accurate identification of the problem in a timely manner; (2) evaluation

and disposition of operability/reportability issues; (3) consideration of extent of condition,

generic implications, common cause, and previous occurrences; (4) classification and

prioritization of the resolution of the problem; (5) identification of root and contributing

causes of the problem; (6) identification of corrective actions; and (7) completion of

corrective actions in a timely manner.

  • December 10, 2009, Unit 3, pipe S31219ML057, T006 Refueling Water Storage

Tank Gravity Feed Outlet

These activities constitute completion of one in-depth problem identification and

resolution sample as defined in IP 71152-05.

b. Findings

No findings of significance were identified.

.5 In-depth Review of Operator Workarounds

a. Inspection Scope

The inspectors conducted a cumulative review of operator workarounds for Units 2 and 3

and assessed the effectiveness of the operator workaround program to verify that the

licensee was: 1) identifying operator workaround problems at an appropriate threshold;

- 48 - Enclosure

2) entering them into the corrective action program; and 3) identifying and implementing

appropriate corrective actions. The review included walkdowns of the control room

panels, interviews with licensed operators and reviews of the control room discrepancies

list, the lit annunciators list, the operator burden list, and the operator workaround list.

These activities constitute completion of one in-depth review of operator workarounds

sample as defined in IP 71152-05.

b. Findings

No findings of significance were identified.

.6 Hours charged for Focused Problem Identification and Resolution Inspection

Hours charged in this report include hours that were expended during the focused

problem identification and resolution inspection, the results of which will be documented

in NRC Inspection Report 05000361; 05000362/2009009.

4OA3 Event Follow-up (71153)

.1 Event Follow Up

a. Inspection Scope

The inspectors reviewed the below listed events for plant status and mitigating actions

to: (1) provide input in determining the appropriate agency response in accordance with

Management Directive 8.3, NRC Incident Investigation Program; (2) evaluate

performance of mitigating systems and licensee actions; and (3) confirm that the

licensee properly classified the event in accordance with emergency action level

procedures and made timely notifications to NRC and state/governments, as required.

  • September 13, 2009, Unit 2, automatic turbine/reactor trip from approximately 94

percent power on low condenser vacuum as a result of a recirculation gate (gate

5) sticking partially open during a planned heat treat evolution

  • September 29, 2009, Unit 2, inspectors follow-up of the fire declared in the

tendon gallery during tendon removal activity

  • October 25, 2009, Unit 3, power transient due to high pressure turbine stop valve

UV2200E failure

  • November 13, 2009, Unit 2, uncontrolled strand uncoiling and anchor head drop

on outside lift system

  • November 18, 2009, Unit 2, incorrectly wired 480 volt 3-phase power cord

resulted in substation J loss of power

  • December 12, 2009, Unit 3, notice of unusual event declared when unit

shutdown commenced for inoperable emergency diesel generators

  • December 23, 2009, Unit 3, unexpected flow degradation for salt water cooling

train A which resulted in a loss of spent fuel pool cooling

- 49 - Enclosure

Documents reviewed by the inspectors are listed in the attachment.

These activities constitute completion of seven inspection samples as defined in

Inspection Procedure 71153-05.

b. Findings

1. Deficiencies Associated with Circulating Water Gate Maintenance

Introduction. The inspectors identified a Green finding for the failure of maintenance

personnel to use Procedure SO23-XV-2, Troubleshooting Plant Equipment and

Systems, in developing procedures and work plans to adequately perform, test, and

communicate maintenance activities on Unit 2 circulating water gate 5.

Description. On September 5, 2009, circulating water gate 5 was manipulated in

preparations for a heat treat of the Unit 2 intake. Gate 5 stuck open at 14 percent during

closure from approximately 40 percent open. Operators in the area of gate 5 noted that

the gate made a loud noise during closure. The licensee initiated Nuclear Notification

NN 200572373. The heat treat was postponed due to higher than normal seawater

temperatures. Maintenance personnel adjusted a stop nut at the south end of gate 5,

and were able to successfully close it. Operations personnel then successfully jogged

gate 5 approximately 10 percent open on two occasions and declared gate 5 functional.

On September 9, 2009, the heat treat was rescheduled to be performed. During the

attempt to open gate 5, it stuck open at approximately 35 percent. Operations personnel

effectively backed out of the evolution. As a result of operator interviews, the inspectors

discovered that the operating crew performing the heat treat evolution on September 9,

2009, received no information from any source that there had been any previous

problems associated with any of the Unit 2 circulating water gates.

Maintenance personnel indicated that they suspected actuator problems with gate 5 but

lacked spare parts to perform the desired repairs. Maintenance personnel then decided

to remove the necessary actuator parts from Unit 3 and install them on Unit 2.

Operations personnel then successfully jogged Unit 2 gate 5 approximately 10 percent

open and declared gate 5 functional at approximately 6:30 a.m. on September 13, 2009.

The heat treat was rescheduled to be performed during the day shift on September 13,

2009. During the attempt to open gate 5, it stuck open at approximately 45 percent.

Operations personnel were unable to overcome the transient caused by increasing

circulating water temperatures and the subsequent loss of condenser vacuum. The

turbine automatically tripped on low condenser vacuum, which resulted in an automatic

reactor trip. The inspectors noted that corrective maintenance procedures used to repair

gate 5 were ineffective, and the postmaintenance testing performed on gate 5 was also

ineffective in determining functionality.

Procedure SO23-XV-2, Troubleshooting Plant Equipment and Systems, Revision 3,

described the process for troubleshooting and fault analysis of installed plant equipment

and provided the methodology and consistent approach for troubleshooting Critical A

equipment. Circulating water gate 5 was rated as a Critical A component, since it has

been classified as having an effect on nuclear safety, plant reliability, or power

generation, in that its failure could result in a plant trip, as well as a 5 percent or greater

full load power reduction. The inspectors concluded that maintenance personnel did not

- 50 - Enclosure

have adequate procedures in place, since the standards of Procedure SO23-XV-2 were

not followed to perform corrective maintenance on Unit 2 circulating water gate 5. The

attempts to repair gate 5 were repeatedly unsuccessful due to inadequate planning,

execution, postmaintenance testing, and communication. The inspectors also concluded

that removing parts from Unit 3 in an attempt to make Unit 2 functional was a poor

practice and exhibited poor oversight by maintenance personnel to ensure adequate

spare parts were available to ensure the functionality of plant equipment that could

directly affect plant operations.

The inspectors noted that the root cause evaluation for Nuclear Notification NN

200580999 generated in response to the event addressed procedural deficiencies in the

maintenance and postmaintenance testing of Unit 2 circulating water gate 5, but did not

address the failure of maintenance personnel to adequately communicate their activities

to other interested departments, particularly operations. The licensee generated a new

notification (Nuclear Notification NN 200718204) to address this deficiency.

Analysis. The failure of maintenance personnel to have adequate procedures in place to

perform maintenance activities on recirculating water gates is a performance deficiency.

The finding is greater than minor because the performance deficiency was a precursor to

a significant event (reactor trip). Using the Manual Chapter 0609, Significance

Determination Process, Phase 1 Worksheets, the finding is determined to have very low

safety significance because the finding did not contribute to both the likelihood of a

reactor trip and the likelihood that mitigation equipment or functions would not be

available. The finding has a crosscutting aspect in the area of human performance

associated with work control because maintenance personnel failed to incorporate

actions to address the need for work groups to communicate, coordinate, and cooperate

with each other during activities in which interdepartmental coordination is necessary to

assure plant and human performance H.3(b).

Enforcement. No violation of regulatory requirements occurred because the finding

occurred on nonsafety, but risk significant secondary plant equipment. The licensee

entered the finding into the corrective action program as Nuclear Notifications NNs

200580999 and 200718204: FIN 05000361/2009005-07, Inadequate Circulating Water

System Maintenance Procedures Contribute to Unit 2 Inadvertent Reactor Trip.

2. Deficiencies Associated with Circulating Water Gate Operation

Introduction. The inspectors identified a Green finding for the failure of operations

personnel to perform an adequate pre-job brief in accordance with procedural

requirements for a planned Unit 2 heat treat evolution.

Description. Unit 2 experienced an automatic turbine/reactor trip from approximately

94 percent power on low condenser vacuum on Sunday, September 13, 2009. The low

vacuum was caused by increasing circulating water temperature as a result of a

recirculation gate (gate 5) sticking partially open during a planned heat treat evolution.

The heat treat evolution is normally performed at approximately six week intervals on

each unit by realigning circulating water to increase temperature in the respective units

intake to clear out unwanted marine life to prevent clogging of the intake structure and

ultimately the salt water cooling/component cooling water heat exchanger.

- 51 - Enclosure

This evolution had been attempted the previous Wednesday, September 9, 2009, and

was successfully aborted without a significant plant transient when a similar problem

occurred on gate 5.

During the event on September 13, 2009, gate 5 failed after it had opened 45 percent.

Gates 4 and 6 were also being opened and gate 3 was being closed simultaneous to the

operation of gate 5. When gate 5 failed at 45 percent open, gates 3 and 4 were 50

percent open and gate 6 was 60 percent open. The personnel operating the gates

indicated that they were confused as to which procedural direction applied, since two

gates were at 50 percent, one was less than 50 percent, and one was greater than 50

percent. The field operator suggested gate 5 be manually jogged to verify overload

status. When gate 5 failed to move, and after an approximate three minute delay,

direction was provided from the control room to close gate 3 and open gate 4. The

inspectors determined that the delay in properly reacting to the failure of gate 5

contributed to the escalation of circulating water temperatures which contributed to the

turbine/reactor trip.

The inspectors reviewed Procedure SO23-5.1.1, Heat Treating the Circulating Water

System, Revision 22, as part of their event follow-up and determined that the guidance

for reacting to circulating water gate failures contributed to the turbine/reactor trip on

Unit 2 on September 13, 2009. Specifically, Procedure SO23-5-1.1, Attachment 8,

Step 2.4 stated:

If any gate stops moving mid-position, utilize the following strategy:

  • If the gates have traveled <50 percent, all movement should be stopped and the

functioning gates restored to their previous positions. The non-functioning gate

should be repaired and restored to its previous position.

  • If the gates have traveled >50 percent, allow gate movement to continue. The non-

functioning gate should be repaired and placed in the intended position.

The inspectors considered the attempts to troubleshoot the cause of the gate failure, and

determine overload status, to be contrary to the Gate Failure Strategy in Procedure

SO23-5-1.1, Attachment 8, which repositions the functioning gates first and dictates no

actions for attempting to troubleshoot or determine the problem with a non-functioning

gate.

Through interviews of licensee personnel, the inspectors reconstructed the pre-job briefs

which took place prior to the commencement of heat treat evolutions on September 9,

2009, and September 13, 2009, and compared them with the requirements of Procedure

OSM-6, Operations Department Human Performance Tools, Revision 8.

The inspectors noted that Procedure OSM-6, Step 3.7.10 stated, in part, to ensure

elements of an effective Pre-job Brief are addressed if required. Under Elements of an

Effective Pre-job Brief, Procedure OSM-6 stated, in part, that the pre-job brief leader

discusses Safety Concerns, Operating Experience, Potential Problems, Error-likely

Situations, Back out Criteria, Communications. The inspectors noted that the

September 9, 2009, pre-job brief included specific requirements to back out of the

evolution should a problem with gate operation occur. The gate operator was explicitly

told to immediately shut gate 3 and open gate 4 should gate 5 stick in place during

opening without delaying to call the control room. Additionally, this back out criteria was

- 52 - Enclosure

reiterated when one of the equipment operators asked for clarification during the pre-job

brief. The inspectors also noted that although potential problems with gate 5 operation

were discussed, no such clarification on back out criteria took place during the

September 13, 2009, pre-job brief. The inspectors concluded that the lack of specificity

during the September 13, 2009, pre-job brief contributed to the delay in operator actions

which ultimately resulted in a turbine/reactor trip on low condenser vacuum due to high

circulating water temperatures. The inspectors therefore concluded that elements of an

effective pre-job brief were not performed in accordance with procedural requirements

on September 13, 2009.

The inspectors noted that the root cause evaluation for Nuclear Notification NN

200580999 generated in response to the event addressed this deficiency.

Analysis. The failure of operations personnel to follow procedural requirements for

conducting an adequate pre-job brief was a performance deficiency. The finding is

greater than minor because the performance deficiency was a precursor to a significant

event (reactor trip). Using the Manual Chapter 0609, Significance Determination

Process, Phase 1 Worksheets, the finding is determined to have very low safety

significance because the finding did not contribute to both the likelihood of a reactor trip

and the likelihood that mitigation equipment or functions would not be available. The

finding has a crosscutting aspect in the area of human performance associated with

resources because the licensee failed to provide adequate procedural guidance to

ensure that operations personnel could safely perform plant evolutions H.2(c).

Enforcement. No violation of regulatory requirements occurred because the finding

occurred on nonsafety, but risk significant secondary plant equipment. The licensee

entered the finding into the licensees corrective action program as Nuclear Notification

NN 200580999: FIN 05000361/2009005-08, Unit 2 Heat Treat Pre-job Brief Not

Performed in Accordance with Procedural Requirements.

3. Fires in Tendon Gallery

Introduction. Three examples of a self-revealing Green noncited violation of Technical

Specification 5.5.1.1.d, were identified for the failure of contractor personnel to properly

implement the requirements of a fire protection procedure for the control of hot work

activities.

Description. The inspectors reviewed a series of hot work related events that were all

associated with the Unit 2 Cycle 16 steam generator replacement outage during pre-

outage and outage work activities. These events involved a failure to properly

implement the hot work procedural requirements of Procedure SO123-XV-1.41, Control

of Ignition Sources, Revision 13. All of the events required fire department response.

On September 1, 2009, a fire was reported associated with hot work activities during

replacement and welding of instrument air lines. The cause was determined to be a

failure of contractor personnel to follow hot work procedural requirements, including poor

housekeeping which allowed combustible material to be near the ignition source that

resulted in a fire. This event was documented in Nuclear Notification NN 200567213.

The other two events were associated with hot work activities during containment tendon

detensioning and removal. The containment tendons are designed as part of the Unit 2

containment structure and are comprised of a bundle of 55, 3/8-inch diameter steel

- 53 - Enclosure

strands. The bundle of strands are enclosed by a 6-inch diameter metal sheath and

filled with grease. Each strand is anchored with a wedge to carry the tensile load.

Detensioning and removal required the cutting of each tendon strand to access each

anchor wedge. The process required that contractor personnel cut each individual

strand with a hand grinder and then apply a hot flame to the exposed strand using an

acetylene torch. This resulted in hot liquefied grease and slag which needed to be

immediately collected into a sand filled metal drum to allow the hot materials to cool.

The licensees fire protection procedure for hot work, Procedure SO123-XV-1.41, did not

allow combustible materials within 35 feet of the ignition source or flame. Because of

the containment tendon detensioning and removal process, and the hot liquefied grease

and slag that was produced, it was not practical to maintain the combustible materials at

the required distance from the ignition sources or flames. Therefore, a flame permit

deviation assessment was required by fire protection engineering. Although a hot work

permit was issued, the requirements of the hot work permit were not followed, in that, the

appropriate fire protection engineering evaluation and deviation assessments were not

completed.

The first event associated with containment tendon activities occurred on September 28,

2009, when a fire was reported in the tendon gallery. This event was documented in

Nuclear Notification NN 200601793. Following the September 28 event, Nuclear

Notification NN 200602213 documented observations where no fire watch was present

to observe the sparks that were occurring during the tendon cutting process. The

nuclear notification failed to identify that uncovered combustible materials were within 35

feet of the observed sparks, and the appropriate evaluations had not been performed.

Further, the only immediate action taken, as documented in the nuclear notification, was

to have the contractor personnel communicate the fire watch inadequacies to their

supervisor. The second event associated with these activities occurred the next day, on

September 29, when a fire event was declared in the tendon gallery. The fire was

extinguished after several attempts, however, due to heat buildup, smoke continued to

fill the tendon gallery area. Workers evacuated the area and the fire department was

contacted. The fire department responded to the event and operations personnel

implemented abnormal operating instruction Procedure SO123-13-21, Fire,

Revision 13. The fire was officially declared out within 8 minutes. This event was

documented in Nuclear Notification NN 200602881.

The direct cause evaluation associated with Nuclear Notification NN 200602881,

concluded that contractor personnel were not complying with the licensees Fire

Protection Program procedures, in that, outage related hot work was authorized even

though the ignition source was in direct contact with combustible material (liquefied

tendon grease) without an approved deviation as required by Procedure

SO123-XV-1.41, Control of Ignition Sources.

Analysis. The failure to properly implement the fire protection procedure was a

performance deficiency. The finding is greater than minor because it is associated with

the protection against external factors (fires) attribute of the Initiating Events

Cornerstone and affects the cornerstone objective to limit the likelihood of those events

that upset plant stability and challenge critical safety functions during shutdown as well

as power operations. Additionally, if left uncorrected, the practice of conducting hot work

in a manner that results in unintended combustion of nearby materials would have the

potential to lead to a more significant safety concern in that it could result in a fire in or

- 54 - Enclosure

near risk significant equipment. Manual Chapter 0609, Appendix M, Significance

Determination Process Using Qualitative Criteria, was used since Appendix F, Fire

Protection Significance Determination Process, does not address the potential risk

significance of shutdown fire protection findings, and Appendix G, Shutdown Operations

Significance Determination Process, does not address fire protection findings. The

NRC management review was performed by using the Manual Chapter 0609,

Appendix F, Phase 1 Worksheet, to establish a bounding analysis. Using the bounding

analysis, the finding is determined to have very low safety significance because the

finding represented a low degradation rating, in that, it did not have any significant effect

on the likelihood that a fire might occur, or that a fire which does occur might not be

promptly suppressed. This finding has a crosscutting aspect in the area of human

performance associated with work practices because the licensee failed to ensure

supervisory and management oversight of work activities, including contractors, such

that nuclear safety was supported H.4(c).

Enforcement. Technical Specification 5.5.1.1.d requires that written procedures be

established, implemented, and maintained covering Fire Protection Program

implementation. The Fire Protection Program was implemented, in part, by Procedure

SO123-XV-1.41, Control of Ignition Sources, Revision 13. Procedure SO123-XV-1.41,

Steps 6.1.1 and 6.4.1.3, required that combustible materials be covered or stored at a

distance of 35 feet from the ignition sources or flames, or that an evaluation be

performed and compensatory actions implemented if this was not practical. Contrary to

the above, between September 1 and September 29, 2009, three examples were

identified where contractor personnel failed to properly implement the requirements of

Procedure SO123-XV-1.41, steps 6.1.1 and 6.4.1.3. Specifically, contractor personnel

failed to ensure that combustible materials were covered or stored at a distance of 35

feet from the ignition source or flame, and no compensatory evaluation was performed.

All three examples of this performance deficiency resulted in a fire. Because this finding

is of very low safety significance and has been entered into the licensees corrective

action program as Nuclear Notification NN 200604378, this violation is being treated as

a noncited violation, consistent with Section VI.A of the NRC Enforcement Policy: NCV

05000361/2009005-09, Failure to Implement Fire Protection Plan Requirements

Related to Hot Work Activities.

4. Notice of Unusual Event

On December 7, 2009, emergency diesel generator train B was declared inoperable

after a monthly surveillance run due to an excessive lube oil system leak (NCV

05000361;05000362/2009005-05). After performing maintenance on the lube oil

system, the monthly surveillance run was performed as a postmaintenance test on

December 9. Nuclear Notification NN 200699513 documents that a low lube oil

temperature alarm was received during this postmaintenance run. Following the

temperature alarm, the emergency diesel generator train B run was stopped and the

generator was declared inoperable but functional. Troubleshooting determined that the

low lube oil temperature switch was sticking and the decision was made to repair the

switch after the diesel generator was restored to operable status. On December 10,

emergency diesel generator train B was declared operable after a satisfactory monthly

surveillance run.

On December 11, 2009, work was conducted under Nuclear Maintenance Order NMO

800422054 to replace the low lube oil temperature switch for emergency diesel

- 55 - Enclosure

generator train B. During the switch replacement, a technician inadvertently grounded a

wire that in turn blew the fuse on the annunciator alarm panel. The emergency diesel

generator train B was immediately declared inoperable. After the fuse was replaced the

emergency diesel generator train B remained inoperable because engineering personnel

determined, due to system design, that the grounded wire by itself should not have

caused the fuse to fail.

On December 12, 2009, operations personnel attempted to start emergency diesel

generator train A in order to rule out a common cause failure in accordance with

Technical Specification 3.8.1, Condition B.3.2. However, emergency diesel generator

train A failed to start and was declared inoperable; this was documented in Nuclear

Notification NN 200704606.

At 1:26 a.m. on December 12, the licensee declared a Notice of Unusual Event as

operations personnel initiated a down power of Unit 3 in accordance with Technical

Specification 3.8.1, Condition F.1, which required the unit to be in Mode 3 within six

hours. At 5:11 a.m., the down power was suspended at 40 percent power after the

emergency diesel generator train B was declared operable based on a successful

operability run and a prompt operability determination. The licensee exited the Notice of

Unusual Event at 6:45 a.m.

Troubleshooting on emergency diesel generator train A determined that voltage noise

from a degraded annunciator power supply incorrectly closed contacts in the speed

switch, which in turn prevented the generator from starting. The inspectors noted that

the emergency diesel generator train A had potentially been inoperable since the last

surveillance run on November 23, 2009. The annunciator power supplies were replaced

and the emergency diesel generator train A was declared operable on December 15,

2009.

Findings associated with this event are documented in Section 1R12.

.2 Event Report Review

a. Inspection Scope

The inspectors reviewed the five below listed licensee event reports and related

documents to assess: (1) the accuracy of the licensee event report: (2) the

appropriateness of corrective actions; (3) violations of requirements; and (4) generic

issues.

b. Observations and Findings

1. (Closed) Licensee Event Report 05000361; 05000362/2008-007-00, Failure to Comply

with TS Surveillance Requirement Completion Time

On September 18, 2008, the licensee identified a practice that did not satisfy a technical

specification condition requirement. Technical Specification 3.8.1, Condition B, requires

Surveillance Requirement 3.8.1.1, AC Sources Verification, be performed within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />

after declaring an emergency diesel generator inoperable, and once per 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />

thereafter. Contrary to this requirement, operations personnel performed Surveillance

Requirement 3.8.1.1 within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> prior to declaring an emergency diesel generator

inoperable for planned periods of inoperability, and once per 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> thereafter. This

- 56 - Enclosure

practice was consistent with the original technical specification but not with the improved

technical specification (implemented August 5, 1996). The implementing procedure for

this surveillance was not revised at the time of implementing the new improved technical

specification. This procedure has been corrected. This failure to comply with

Surveillance Requirement 3.8.1.1 completion time constitutes a violation of minor

significance that is not subject to enforcement action in accordance with the NRCs

Enforcement Policy. This licensee event report is closed.

2. (Closed) Licensee Event Report 05000361/2008-005-00, Missed Surveillance and Plant

Mode Change Causes TS Violation

On June 9, 2008, Unit 2 entered Mode 2 from Mode 3 during plant startup. At about

1443 PDT, the control room supervisor recognized that the control element assembly

alignment Surveillance Requirements 3.1.5.1 and 3.1.5.2 had not been completed prior

to the mode change. Technical Specification 3.1.5 is applicable in Modes 1 and 2, but

not in Mode 3. This was a violation of Surveillance Requirement 3.0.4 which prevents

mode entry without completing all applicable surveillance requirements. Operations

personnel completed the surveillances with satisfactory results. The procedure for the

mode change was not clear and has been revised to specifically require that the

surveillances are completed. This failure to comply with technical specification

Surveillance Requirement 3.0.4 constitutes a violation of minor significance that is not

subject to enforcement action in accordance with the NRCs Enforcement Policy. This

licensee event report is closed.

3. (Closed) Licensee Event Report 05000361/2009-001-00, Unit Trip on Low Vacuum

Caused by Intake Circulating Water Gate

San Onofre Unit 2 experienced an automatic turbine/reactor trip from approximately

94 percent power on low condenser vacuum on September 13, 2009. The low vacuum

was caused by increasing circulating water temperature as a result of a recirculation

gate (gate 5) sticking partially open during a planned heat treat evolution. Findings

associated with this event are described Section 4OA3 of this report. This licensee

event report is closed.

4. (Closed) Licensee Event Report 05000361/2007-005-00, Loose Electrical Connection

Results in Inoperable Pump Room Cooler

On March 1, 2007, the Unit 2 spent fuel pool pump room emergency air conditioning fan

was started for air flow measurement and tripped on thermal overload. The phase A

connection to the thermal overload was found to be loose with evidence of arcing. The

licensee determined the loose connection likely was caused by inadequate tightening of

the connection during maintenance on October 27, 2006. Since the backup cooling for

this room was operable and the room temperature did not exceed the design

temperature, the spent fuel pool pump remained operable. Findings associated with this

licensee event report review are described Section 4OA5.4 of this report. This licensee

event report is closed.

5. (Closed) Licensee Event Reports 05000361; 05000362/2007-006-00 and 05000361;

05000362/2007-006-01, Loose Electrical Connection Results in One Train of

Emergency Chilled Water (ECW) System Inoperable

- 57 - Enclosure

On June 9, 2007, operations personnel found the control panel for emergency chiller

E336 de-energized. Further investigation identified that the retaining screw anchoring

the cable to the supply breaker in the power panel was stripped, preventing the cable

from being secured tightly. The licensee concluded that the loose connection was most

likely due to over tightening the terminal screw on June 28, 2005, when the breaker was

replaced. Findings associated with this licensee event report review are described

Section 4OA5.4 of this report. This licensee event report is closed.

4OA5 Other Activities

.1 Quarterly Resident Inspector Observations of Security Personnel and Activities

a. Inspection Scope

During the inspection period, the inspectors performed observations of security force

personnel and activities to ensure that the activities were consistent with San Onofre

Nuclear Generating Station security procedures and regulatory requirements relating to

nuclear plant security. These observations took place during both normal and off-normal

plant working hours.

These quarterly resident inspector observations of security force personnel and activities

did not constitute any additional inspection samples. Rather, they were considered an

integral part of the inspectors normal plant status review and inspection activities.

b. Findings

No findings of significance were identified.

.2 Temporary Instruction 2515-175, Emergency Response Organization, Drill/Exercise

Performance Indicator, Program Review

a. Inspection Scope

The inspector performed Temporary Instruction 2515-175, Emergency Response

Organization, Drill/Exercise Performance Indicator, Program Review, ensured the

completeness of Attachment 1 to the Instruction, and forwarded the data to NRC

Headquarters.

b. Findings

No findings of significance were identified.

.3 Temporary Instruction 2515-172, Reactor Coolant System Dissimilar Metal Butt Welds

a. Inspection Scope

The reactor coolant system for this unit is carbon steel with stainless steel cladding and

has the following dissimilar metal welds subject to the requirements of the Materials

Reliability Program-139:

1. Two 12-inch pressurizer surge line nozzles were mitigated during a previous

outage using a weld overlay process. Both welds were classified as

Category F per material reliability program guidelines.

- 58 - Enclosure

2. Three 6-inch pressurizer safety nozzles were mitigated during a previous

outage using a weld overlay process. Both welds were classified as

Category F per materials reliability program guidelines.

3. One 4-inch pressurizer spray nozzle was mitigated during a previous outage

using a weld overlay process. The weld was classified as Category F per

materials reliability program guidelines.

4. One 16-inch shutdown cooling nozzle was mitigated during a previous outage

using a weld overlay process. The weld was classified as Category F per

materials reliability program guidelines.

5. Four 12-inch emergency core cooling system injection nozzles were

previously left unmitigated. The licensee performed a volumetric inspection

of each nozzle during the current outage and classified the welds as

Category I per materials reliability program guidelines.

6. Four 30-inch reactor coolant pump inlet nozzles (unmitigated as of this

outage). The licensee performed a volumetric inspection of each nozzle

during the current outage and classified the welds as Category I per materials

reliability program guidelines.

7. Four 30-inch reactor coolant pump outlet nozzles (unmitigated as of this

outage). The licensee performed a volumetric inspection of each nozzle

during the current outage and classified the welds as Category I per materials

reliability program guidelines.

All of the pressurizer and hot-leg-temperature welds have been mitigated, in previous

outages, using a full-structural overlay weld. The cold-leg-temperature welds have not

been mitigated as of this outage. The cold-leg welds have been, or will be,

volumetrically inspected and any decision to mitigate these welds will be made on the

basis of these inspections.

03.01 Licensees Implementation of the Materials Reliability Program-139 Baseline

Inspections

a. The inspector reviewed records of structural weld overlays and

nondestructive examination activities associated with the licensees

pressurizer structural weld overlay mitigation effort. The inspector observed

nondestructive examination activities associated with one cold leg weld that

was not overlaid.

b. The licensee was not planning to take any deviations from the baseline

inspection requirements of Materials Reliability Program-139, and all other

applicable dissimilar metal butt welds were scheduled in accordance with

Materials Reliability Program-139 guidelines.

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03.02 Volumetric Examinations

a. The inspector observed the ultrasonic examination of one cold leg weld that

was not scheduled to be overlaid. This examination was conducted in

accordance with ASME Code,Section XI, Supplement VIII Performance

Demonstration Initiative requirements regarding personnel, procedures, and

equipment qualifications. No relevant conditions were identified during this

examination.

b. The inspector reviewed records for the nondestructive evaluations performed

on one pressurizer surge line weld overlay. Inspection coverage met the

requirements of Materials Reliability Program-139 and no relevant conditions

were identified.

c. The certification records of ultrasonic examination personnel were reviewed

for those personnel that performed the examinations of the pressurizer and

cold-leg welds. All personnel records showed that they were qualified under

the EPRI Performance Demonstration Initiative.

d. No deficiencies were identified during the nondestructive examinations.

03.03 Weld Overlays

a. The inspector reviewed the welding activities associated with the weld

overlay performed on the pressurizer surge line nozzle.

b. The licensee submitted and received NRC authorization for the use of relief

request from the ASME code to apply weld overlays on their dissimilar metal

butt welds. Using this, the licensee performed weld overlays on all of the

dissimilar metal butt welds associated with pressurizer and hot leg

temperatures. This welding took place in previous outages. The inspector

reviewed the weld records for one of these welds to ensure the welding was

performed in accordance with the ASME code, as modified by the approved

relief requests.

c. Deficiencies have not been identified in the completed full structural weld

overlays.

03.04 Mechanical Stress Improvement

This item was not applicable because the licensee did not have plans to employ

a mechanical stress improvement process.

03.05 Inservice inspection program

The inspector reviewed the licensees risk informed inservice plan and verified

that all dissimilar metal butt welds have been entered into the plan and will be

examined on a schedule consistent with Materials Reliability Program-139.

b. Findings

No findings of significance were identified.

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.4 (Closed) Unresolved Item 05000361;05000362/2008013-07, Degraded Electrical

Connections

a. Inspection Scope

The inspectors evaluated Unresolved Item 05000361;05000362/2008013-07,

Degraded Electrical Connections.

b. Findings

Introduction. The inspectors identified a Green noncited violation of 10 CFR Part 50,

Appendix B, Criterion III, Design Control, with thirteen examples for the failure of the

licensee to ensure that appropriate measures were in place to assure that systems

specified in the design basis were maintained in a configuration which provided a

reasonable assurance of operability during design basis events.

Description. Details associated with this unresolved item were described in

Section 2.2.1 of NRC Inspection Report 05000361; 05000362/2008013 and are

summarized in the table below.

Table 1: Identified Loose Electrical Connections

Item Equipment Description Condition

1 3A276 Emergency Diesel Generator 3G003 Failed to start;

Building Supply Fan (3BH11) Discovered June

2005

2 3A277 Emergency Diesel Generator 3G002 2 loose connections;

Building Supply Fan (3BH12) Discovered June

2005

3 E549 Emergency Diesel Generator 3G002 Discovered June

Radiator Fan (3BH07) 2005

4 2BY37 Fuel Handling Building Pump Room Failed to run;

Emergency Air Conditioning Discovered March

Unit E441 Feeder Breaker 2007

5 2BJ06 Safety Injection Tank 2T008 to Documented January

Reactor Coolant Loop 1A Valve 2HV9340 2006

6 3BE06 Auxiliary Feedwater to Steam Generator 3 loose connections;

Control Valve 3HV4713 Discovered August

2005

7 2BY30 Component Cooling Water Building Loose grounding wire

Pump Room Emergency AC Unit E453 in MCC bucket;

Discovered July 2005

8 2BE11 Safety Injection Tank T009 to Reactor 3 loose connections;

Discovered January

- 61 - Enclosure

Table 1: Identified Loose Electrical Connections

Coolant Loop 2A Valve 2HV9360 2006

9 BS09 Control Building Control Room Loose connection in

Emergency Air Supply Fan A206 indicator circuit;

Discovered February

2006

10 2/3ME336 Emergency Chiller Supply Breaker E336 Instrumentation panel

failed; Discovered

June 2007

11 2B008 125 VDC Battery 2D2 Loose connection on

bus bar; Discovered

September 2007

12 3RY7870 Condenser Air Ejector Wide Range Failed Surveillance;

Radiation Monitor Discovered June

2008

13 3BD21 Diesel Radiator Fan 3E550 Feeder Degraded

Breaker connection;

Discovered July 2008

Analysis. The failure to ensure the integrity of electrical connections in equipment which

may be called upon during design basis events was a performance deficiency. The

finding is greater than minor because it is associated with the equipment performance

attribute of the Mitigating Systems Cornerstone and affects the associated cornerstone

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. In accordance with Manual

Chapter 0609, Attachment 4, Table 4a, Question 5, a Phase 3 analysis was required

because the finding screened as potentially risk significant due to a seismic, flooding, or

severe weather initiating event. In accordance with Inspection Manual Chapter 0609,

Appendix A, the analyst determined that the conditions documented in Table 1 of this

inspection report should be evaluated as a single inspection finding because they

resulted from a common cause.

Internal Initiators:

The analyst evaluated Conditions 2, 3, 5 through 9, 11, and 13 documented in Table 1.

While the conditions of the fasteners were degraded, none of these components were

found to be in a failed condition. Therefore, there was no impact to internal initiated risk.

The remainder of the conditions documented on Table 1 was evaluated as discussed

here:

Condition 1: This condition involved the failure of the building supply fan for emergency

diesel generator 3G003 to start on demand in June, 2005. This fan was one of two

redundant fans performing the same function. However, to bound the change in risk, the

analyst conducted a Phase 3 analysis assuming the failure of emergency diesel

- 62 - Enclosure

generator 3G003, using the plant-specific SPAR model. The CDF (Core Damage

Frequency) for a failed diesel generator was 1.9 x 10-5/year. The exact time of failure

was unknown, but the fan had worked properly during a surveillance test approximately

30 days earlier. Therefore, the analyst assumed the diesel had been failed for 15 days.

This resulted in a bounding CDF of 7.8 x 10-7 over a 15-day period.

The analyst noted that this was a bounding evaluation of a specific postulated failure and

was not appropriate to combine with the risk of other evaluations performed. The

analyst determined qualitatively that this condition would not have greatly increased the

overall risk of the finding.

Condition 4: This condition involved the failure of the fuel handling building pump room

emergency air conditioning unit feeder breaker E441. The failure of this breaker

potentially affected the functionality of its associated spent fuel pool cooling pump.

Given the volume of water stored in the spent fuel pool, the low heat loading of fuel in

the pool, the availability of makeup systems, and the other train of spent fuel pool

cooling, the analyst determined that this condition did not greatly affect the core damage

frequency.

Condition 10: This condition involved the inoperability of the train A emergency chilled

water system chiller ME336 discovered on June 9, 2007 and reported by the licensee in

LER 2-2007-006-001. The licensees investigation of the cause of control panel (L177)

for ME336 being found de-energized on June 9, 2007 revealed that a power cable was

pulled out of the feeder breaker in a separate panel (Q033) supplying 120 VAC to the

chiller control panel, L177. Information provided by the licensee established May 17,

2007 as the date of the last successful surveillance of emergency chilled water train A,

representing a 23 day period that the performance deficiency potentially affected the

plant.

The analysts agreed with the licensee assessment that the subject performance

deficiency would result in the loss of the emergency chilled water train A from a

postulated seismic event that also causes a loss of offsite power. Under such a

scenario, the emergency chilled water system would be required to cool important loads

such as the main control room and critical switchgear and distribution panel rooms on

the 50 foot elevation in the auxiliary building. The inability to successfully dissipate the

heat loads could ultimately result in control room abandonment and the added

complexity of shutting down and cooling down from the remote shutdown panel. The

aggregate of these factors would adversely affect the core damage frequency. To

quantify the increase in core damage frequency (CDF) caused by the condition, the

analysts evaluated the added risk associated with the following circumstances: a)

emergency chilled water system becoming unavailable due to a seismically induced loss

of offsite power (8.0 x 10-7/year); b) emergency chilled water system becoming

unavailable due to internal event initiators (3.3 x 10-6/year); and c) Loss of both

emergency chilled water trains following a postulated loss of offsite power event causing

temperature increases that would necessitate main control room abandonment

(6.0 x 10-6/year).

A one year exposure time was considered appropriate for the seismic event vulnerability

whereas a 12-day (T/2 + repair time) exposure time was applied in the analysis of

internal event initiators and main control room abandonment. Considering the total loss

of emergency chilled water (train A loss due to the performance deficiency and nominal

- 63 - Enclosure

failure probability loss of train B) the change in core damage probability, assuming that

the above postulated conditions occurred, was calculated as follows:

CDF = (8.0 x 10-7/yr * 1 yr) + (3.3 x 10-6/yr * 12/365 yrs) + (6.0 x 10-6/yr * 12/365 yrs)

= 8.0 x 10-7 + 1.1 x 10-7 + 6.2 x 10-8

= 9.7 x 10-7

The analyst noted that the core damage sequences associated with this condition

resulted in loss of equipment from overheating. Therefore, the risk associated with this

condition was not considered additive to the bounding analyses conducted for the other

conditions.

Condition 12: This condition involved the condenser air ejector wide range radiation

monitor. The loose termination was discovered when recorder Point 9 was found out of

specification during a required 92-day surveillance. This recorder point had been found

high, but within the acceptable range, during the previous surveillance. Therefore, the

analyst assumed the point drifted out of specification, purportedly because of the loose

termination, at some time during the 92-day interval. The licensee stated that the

monitor does not perform any automatic isolation, control or alarm function, nor is the

monitor referenced in the decision logic for abnormal or emergency procedures. As

such, failure would not directly affect the core damage frequency. Additionally, although

the point was indicating high, it would have indicated a trend had a primary to secondary

leak developed.

External Initiating Events:

Seismic

Using a method similar to that documented in Attachment 3 of NRC Inspection Report

05000361/2008013; 05000362/2008013, the analyst evaluated the impact of the

Conditions 1 through 9 and 11 through 13 listed in Table 1 for their impact to risk during a

seismic event. Assuming that the loose connections listed doubled the probability that

the associated motor-control center would fail as a result of a seismic event, the analyst

quantified the seismic impact. The frequency of a seismically induced failure occurring

simultaneous with a nonrecoverable loss of offsite power was calculated to be

1.8 x 10-4/year. Based on an evaluation of the equipment redundancy and safety

function of each condition, the analyst determined that the worst case failure would be

the loss of a single diesel generator. The conditional core damage probability for this

was quantified as 2.0 x 10-3. Therefore, the analyst estimated the worst case failure at a

CDF of 3.6 x 10-7. The analyst determined that the probability of failure of more than

one of the components in the correct combination to increase the core damage

frequency significantly would be very low.

High Winds, Floods, and Other External Events

The analyst reviewed the IPEEE and determined that no other credible scenarios

initiated by high winds, floods, fire, and other external events could initiate a loss of

offsite power and directly cause the perturbation of the thirteen conditions associated

with this finding. Therefore, the analyst concluded that external events other than

seismic events were not significant contributors to risk for this finding.

- 64 - Enclosure

Large Early Release Frequency

In accordance with the guidance in NRC Inspection Manual Chapter 0609, Appendix H,

this finding would not involve a significant increase in risk of a large early release of

radiation because San Onofre has a large, dry containment and the accident sequences

contributing to a change in the core damage frequency did not involve either a steam

generator tube rupture or an intersystem loss of coolant accident.

As a combined result of these evaluations, the analyst determined that this finding was

of very low safety significance (Green).

The finding has a crosscutting aspect in the area of human performance associated with

resources for the failure to maintain complete, accurate, and up-to-date design

documentation, procedures, and work packages H.2(c).

Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,

Criterion III, Design Control, states, in part, that measures shall be established to

assure that applicable regulatory requirements and the design basis, as defined in

§ 50.2 and as specified in the license application, for those structures, systems, and

components to which this appendix applies are correctly translated into procedures and

instructions. These measures shall include provisions to assure that appropriate quality

standards are specified and included in design documents. Contrary to this requirement,

between June 2005 and July 2008, the licensee failed to ensure that appropriate

measures were in place to assure that systems specified in the design basis were

maintained in a configuration which provided a reasonable assurance of operability

during design basis events. Specifically, thirteen examples of safety-related equipment

were identified with electrical connections that were not maintained in the required

design configuration.

Because this finding is of very low safety significance and has been entered into the

licensees corrective action program as Action Requests ARs 050601315, 050601324,

060101159, 070200254, 200066209, Nuclear Notifications NNs 200089167, 200058371,

200100730, and Corrective Action Order 800126624, this violation is being treated as a

noncited violation, consistent with Section VI.A of the NRC Enforcement Policy: NCV

05000361;05000362/2009005-10, Inadequate Design Control for Safety-Related

Electrical Connections.

4OA6 Meetings

Exit Meeting Summary

On September 25, 2009, the inspectors presented the results of the onsite inspection of the

2009 emergency preparedness exercise, and the inspection of licensee changes to their

emergency plan and emergency action levels to Mr. R. Ridenoure, Senior Vice President and

Chief Nuclear Officer, and other members of the licensees staff. The licensee acknowledged

the issues presented.

On October 16, 2009, the inspector presented the in-service inspection results to Mr. D. Bauder,

Plant Manager, and other members of the licensee staff. The licensee acknowledged the issues

presented.

- 65 - Enclosure

On October 29, 2009, the inspector conducted a telephonic exit meeting to present the results of

the in-office inspection of changes to the licensees emergency action levels to Mr. B. Ashbrook,

Manager, Onsite Emergency Preparedness. The licensee acknowledged the issues presented.

On October 30, 2009, the inspectors presented the radiation safety inspection results to

Mr. A. Hochevar, Station Manager, and other members of the licensee staff. The licensee

acknowledged the issues presented.

On December 15, 2009, the inspector briefed Mr. Bill Arbour, Training Supervisor, of the results

of the annual licensed operator requalification program inspection. The licensee acknowledged

the issues presented.

On January 13, 2010, the inspectors presented the integrated inspection results to

Mr. R. Ridenoure, Senior Vice President and Chief Nuclear Officer, and other members of the

licensee staff. The licensee acknowledged the issues presented.

The inspectors asked the licensee whether any materials examined during the inspections

should be considered proprietary or sensitive. The inspectors returned or destroyed all

proprietary information reviewed during the inspections and all identified sensitive information

has been returned to the appropriate licensee custodian.

4OA7 Licensee-Identified Violations

The following violations of very low safety significance (Green) were identified by the licensee

and are violations of NRC requirements which meet the criteria of Section VI of the NRC

Enforcement Policy, NUREG-1600, for being dispositioned as noncited violations.

.1 On August 8 and August 9, 2009, the licensee failed to follow their emergency plan in

that during one full shift and 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> 46 minutes of another shift the emergency plan-

required electrical maintenance position was not staffed. This finding is a failure to

comply with an NRC requirement, is associated with a 50.47(b) Planning Standard, is

not associated with a risk-signifcant Planning Standard, and is not a functional failure of

the planning standard because processes for ensuring the staffing of required on-shift

emergency response organization positions were generally effective. This finding has

been entered into the licensees corrective action program as Direct Cause Evaluation

200535198.

.2 Title 10 of the Code of Federal Regulations 50.65(a)(4), states in part, that before

performing maintenance activities, the licensee shall assess and manage the increase in

risk that may result from the proposed maintenance activities. Contrary to the above,

between September 30, 2009, and December 10, 2009, work control and operations

personnel failed to adequately assess and manage the increase in risk associated with

planned maintenance activities. Specifically, on September 30, errors were inadvertently

introduced to the risk model, such that, the risk assessments for planned maintenance

utilized a safety monitor with nonconservative allowed configuration time values until

discovery of the error on December 10, 2009. This finding has been entered into the

licensees corrective action program as Nuclear Notification NN 200701778. The finding

is of very low safety significance because the incremental core damage probability deficit

and the incremental large early release probability deficit were of sufficiently low

magnitudes.

- 66 - Enclosure

.3 Title 10 of the Code of Federal Regulations, Part 50, Appendix B, Criterion V,

Instructions, Procedures, and Drawings, states, in part, that activities affecting quality

shall be prescribed by documented instructions, procedures, or drawings, of a type

appropriate to the circumstances and shall be accomplished in accordance with these

instructions, procedures, or drawings. Procedure SO123-XV- 50.CAP-1, Writing

Nuclear Notifications for Problem Identification and Resolution, Revision 2, stated that

all personnel identifying problems that have the potential to affect the ability of a

structure, system, or component to perform its specified function will immediately notify

the shift manager or designee, and write a nuclear notification prior to the end of their

shift. Contrary to the above, on November 20, 2009, engineering personnel failed to

initiate a nuclear notification in a timely manner in accordance with their procedures.

Specifically, engineering personnel failed to write a nuclear notification in accordance

with Procedure SO123-XV-50.CAP-1, for a boric acid leak identified on Unit 2 pipe

S21219ML057, T006 RWST Gravity Feed Outlet. This finding has been entered into

the licensees corrective action program as Nuclear Notification NN 200683697. The

finding is of very low safety significance because the finding did not result in an actual

loss of safety function.

This licensee identified violation is another example of NCV 05000361/2009005-01,

Failure to Initiate a Notification in a Timely Manner, and is further discussed in

Section 1R06.1 of this report.

ATTACHMENT: SUPPLEMENTAL INFORMATION

- 67 - Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

T. Adler, Manager, Maintenance/Systems Engineering

B. Arbour, Operator Continuing Training Supervisor

J. Armas, Supervisor, Maintenance Engineering Fluid Process

B. Ashbrook, Manager, Emergency Preparedness

D. Axline, Technical Specialist, Nuclear Regulatory Affairs

D. Bauder, Plant Manager

P. Blakeslee, Supervisor, Mechanical Auxiliary Systems

J. Carey, Technician, Health Physics

S. Chun, Supervisor, Electrical/I&C Systems

B. Corbett, Manger, Performance Improvement

G. Cook, Manager, Compliance, Nuclear Regulatory Affairs

D. Deglopper, ALARA Planner, Health Physics

S. Deines, Technician, Health Physics

P. Elliot, Operations Supervisor, Health Physic Department

R. Elsasser, Manger, Training

M. Farmer, Radioactive Materials Control Supervisor, Health Physics

J. Fee, Manager, Site Emergency Preparedness

K. Gallion, ALARA Supervisor, Health Physics

S. Gardner, Electrical/System Engineering Manager

M. Graham, Manager, Plant Operations

A. Hochevar, Station Manager, Plant Operations

E. Hubley, Director, Maintenance/Construction

G. Johnson, Jr., Senior Nuclear Engineer, Maintenance/Systems Engineering

K. Johnson, Manager, Design Engineering

L. Kelly, Engineer, Nuclear Regulatory Affairs

D. Spires, Director, Work Control

J. Madigan, Manager, Health Physics

J. McGaw, Engineering Supervisor

A. Meichler, Mechanical/System Engineering Supervisor

M. Mihalik, Areva Project Manager, Steam Generator Replacement Project

M. Miranda, Technician, Health Physics

R. Nielsen, Supervisor, Nuclear Oversight

B. MacKissock, Director, Plant Operations

L. Pepple, ALARA Planner, Health Physics

N. Quigley, Manager, Maintenance/System Engineering

R. Richter, Engineering Supervisor, Fire Protection

M. Russell, Technical Specialist, Health Physics

C. Ryan, Manager, Maintenance & Construction Services

R. Sherman, ALARA Planner, Health Physics

R. St. Onge, Director Nuclear Regulatory Affairs

J. Todd, Manager, Security

G. Vechinski, Inservice Inspection/Steam Generator Support Supervisor

D. Wilcockson, Manager of Operations Training

A. Williams, Technician, Health Physics

A-1 Attachment

NRC Personnel

D. Loveless, Senior Reactor Analyst

E. Schrader, Emergency Preparedness Specialist

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000361/2009005-01 NCV Failure to Initiate a Notification in a Timely Manner

(Section 1R06)05000361/2009005-02 NCV Failure to Adequately Identify Problems in Corrective Action

Program (Section 1R06)05000362/2009005-03 NCV Failure to Correct Problems with Emergency Diesel

Generator Train B (Section 1R12)05000362/2009005-04 NCV Failure to Correct Problems with Emergency Diesel

Generator Train A (Section 1R12)05000362/2009005-05 NCV Failure to Follow the Operability Determination Process

(Section 1R15)05000361/2009005-06 NCV Failure to Adequately Implement Compensatory Measures05000362/2009005-06 to Maintain Equipment Operable (Section 1R15)05000361/2009005-07 FIN Inadequate Circulating Water System Maintenance

Procedures Contribute to Unit 2 Inadvertent Reactor Trip

(Section 4OA3)05000361/2009005-08 FIN Unit 2 Heat Treat Pre-job Brief Not Performed in

Accordance with Procedural Requirements (Section 4OA3)05000361/2009005-09 NCV Failure to Implement Fire Protection Plan Requirements

Related to Hot Work Activities (Section 4OA3)05000361/2009005-10 NCV Inadequate Design Control for Safety-Related Electrical

05000362/2009005-10 Connections (Section 4OA5)

Closed

05000361/2008-007-00 LER Failure to Comply with TS Surveillance Requirement

05000362/2008-007-00 Completion Time (Section 4OA3)

A-2 Attachment

Closed

05000361/2008-005-00 LER Missed Surveillance and Plant Mode Change Causes TS

Violation (Section 4OA3)

05000361/2009-001-00 LER Unit Trip on Low Vacuum Caused by Intake Circulating Water

Gate (Section 4OA3)

05000361/2007-005-00 LER Loose Electrical Connection Results in Inoperable Pump

Room Cooler (Section 4OA3)

05000361/2007-006-00 LER Loose Electrical Connection Results in One Train of

05000362/2007-006-00 Emergency Chilled Water (ECW) System Inoperable

05000361/2007-006-01 (Section 4OA3)

05000362/2007-006-01

05000361/2008013-07 URI Degraded Electrical Connections (Section 4OA5)05000362/2008013-07

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

Procedures

NUMBER TITLE REVISION

SO23-13-8 ISS2 Severe Weather 7

Miscellaneous

NUMBER TITLE

UFSAR 2.3 Meteorology NA

UFSAR 3.11 Environmental Design of Mechanical and Electrical NA

Equipment

UFSAR 9.2.6 Condensate Storage and Transfer System NA

A-3 Attachment

Section 1RO4: Equipment Alignment

Procedures

NUMBER TITLE REVISION

SO23-3-2.11 Spent Fuel Pool Operations 26

SO23-3-3.27.2 Surveillance Operating Instruction 19

SO23-2-8 Saltwater Cooling System Operation 32

SO23-2-8.1 Saltwater Cooling Removal and Returning to Service 9

Evaluation

SO23-2-13.1 Diesel Generator Alignment 4

Nuclear Notifications

NUMBER

200657834

Drawings

NUMBER TITLE REVISION

40122A Fuel Pool Cooling System 18

40122B Fuel Pool Cooling System 25

40122C Fuel Pool Cooling System 16

40122X Fuel Pool Cooling System 5

A-4 Attachment

Section 1RO5: Fire Protection

Procedures

NUMBER TITLE REVISION

SO23-XV-4.13 Control of Work and Storage Areas Within the Protected 5

Area

SO23-XIII-4.13 Inspection for Control of Combustibles and Transient Fire 1

Loads

Nuclear Notifications

NUMBER

200602405

Drawings

NUMBER TITLE REVISION

2-001A Pre-Fire Plans 6

2-001 Pre-Fire Plans 4

2/3-019 Pre-Fire Plans 6

2/3-024 Pre-Fire Plans 6

2/3-020 Pre-Fire Plans 6

2/3-025 Pre-Fire Plans 5

2/3-023 Pre-Fire Plans 7

Section 1RO6: Flood Protection Measures

Procedures

NUMBER TITLE REVISION

SO23-V-8.3 External Corrosion and Aging Program 0

Miscellaneous

A-5 Attachment

NUMBER TITLE NA

UFSAR 3.4 Water Level (Flood) Design

Section 1RO8: In-service Inspection Activities

Procedures

NUMBER TITLE REVISION

SO23-XXXIII- Reactor Coolant System Alloy 600 Inspection 7

8.16

SO23- IntraSpect Eddy Current Inspection of Vessel Head 7

XXVII.3.5.1.1 Penetration J-Welds and Tube OD Surfaces

SO23-XV-85 Boric Acid Corrosion Control Program (BACCP) 4

SO23-V-8.15 Containment Boric Acid Leak Inspection 2

SO123-IN-1 Inservice Inspection/Inservice Test Programs 8

S23-XVII-1.1 Inservice Inspection Program Maintenance 5

SO123-XV- SONGS Nuclear Notification Screening 3

50.CAP-2

PQS T4EN51 Non-RCS Alloy 600 Boric Acid Leakage Inspection and 1

Evaluation

PQS T4EN52 RCS Alloy 600 Boric Acid Leakage Inspection and 0

Evaluation

SO23-XXVII- Liquid Penetrant Examination 2

20.48

SO23-XXVII- Procedure for the Phased Array Ultrasonic Examination of 1

33.14 Weld Overlaid Similar and Dissimilar Metal Welds

SO23-XXVII- Ultrasonic Examination of Dissimilar Metal Piping Welds 2

30.9

A-6 Attachment

Section 1RO8: In-service Inspection Activities

PDI-UT-10 PDI Generic Procedure for the Ultrasonic Examination of C

Dissimilar Metal Welds

Nuclear Notifications

NUMBER

200599549 200599604 200599688 200599422 200599618

200599623 200629478 200618073 200633298

Action Requests

NUMBER

071200751 071200830 080401360

Miscellaneous

NUMBER TITLE REVISION / DATE

Letter from R J. Docket Nos. 50-361 and 50-362 Revision 1 to October 2, 2009

St. Onge (SCE) Third Ten-Year Inservice Inspection (151) Interval

to USNRC Relief Request 151-3-29 Inspection of Reactor

Vessel Head Control Element Drive Mechanism

Nozzles San Onofre Nuclear Generating Station

Units 2 and 3

Letter from R J. Docket Nos. 50-361 and 50-362 Third Ten-Year October 2, 2009

St. Onge (SCE) Inservice Inspection (151) Interval Relief Request

to USNRC 151-3-30 Inspection of Reactor Vessel Head In-

Core Instrument Nozzles San Onofre Nuclear

Generating Station Units 2 and 3

Letter from J. CRDM/CEDM Qualifications October 2, 2009

Spanner (EPRI)

to M. McDevitt

(SC&E)

Code Case N- Alternative Examination Requirements for PWR March 28, 2006

729-1 Reactor Vessel Upper Heads With Nozzles Having

Pressure-Retaining Partial-Penetration Welds

Section XI Division 1

A-7 Attachment

Section 1RO8: In-service Inspection Activities

Code Case N- Additional Examinations for PWR Pressure July 5, 2005

722-1 Retaining Welds in Class 1 Components

Fabricated With Alloy 600/82/182 Materials Section

XI Division 1

MRP 2008-066 Letter from J. Hagan (EPRI) to MRP Technical December 17, 2008

Advisory Group Primary System Piping Butt Weld

Inspection and Evaluation Guideline (MRP-139

Revision 1)

MRP 2009-031 Letter from J. Hagan (EPRI) to MRP Technical June 8, 2009

Advisory Group MRP-139 Revision 1 Interim

Guidance on Reconciliation of BMV Requirements

with Code Case N-722 (Mandatory Element)

WR2-08-203 Weld Record for S2-1208-ML-003 (2TSH9205) 0

PQR-68 Manual Welding of Austenitic Stainless Steel January 3, 1985

Materials

PQR-5 Manual Gas Tungsten Arc Welding of Stainless June 28, 1984

Steel Material

WPS 8-GT Manual GTAW of P-Number 8 Austenitic Stainless September 13, 1998

Steel Alloys using IN308L/ER308L or

IN316Ll/ER316L Filler Metals

PQR 08-08-TS- 0

001

PQR-08-08-TS- 0

002

WPS 08-08-TS- 4

001

107294-TR-253 WSI Traveler Replacement of Check Valve MU 0

021

Phased Array SONGS U2 Hot Leg Surge January 11, 2009

Ultrasonic

Examination

Record

02-008-002 SONGS ISI Ultrasonic Calibration/Examination October 6, 2009

A-8 Attachment

Section 1RO8: In-service Inspection Activities

Report Safe End to Elbow Weld

209-16PT-001 Liquid Penetrant Examination Report September 16, 2009

209-16PT-002 Liquid Penetrant Examination Report September 16, 2009

209-16PT-003 Liquid Penetrant Examination Report September 17, 2009

209-16PT-004 Liquid Penetrant Examination Report September 17, 2009

209-16PT-005 Liquid Penetrant Examination Report September 18, 2009

209-16PT-006 Liquid Penetrant Examination Report September 18, 2009

209-16PT-007 Liquid Penetrant Examination Report September 18, 2009

209-16PT-008 Liquid Penetrant Examination Report September 18, 2009

209-16PT-009 Liquid Penetrant Examination Report September 18, 2009

209-16PT-010 Liquid Penetrant Examination Report September 21, 2009

209-16PT-011 Liquid Penetrant Examination Report September 22, 2009

209-16PT-013 Liquid Penetrant Examination Report October 20, 2009

Section 1R11: Licensed Operator Requalification Program

Procedures

NUMBER TITLE REVISION

SO23-3-2.22 Engineered Safety Features Actuation System Operation 18

Miscellaneous

NUMBER TITLE REVISION

RS09C7 2009 Cycle 7b Simulator Summary 0

A-9 Attachment

Section 1R12: Maintenance Effectiveness

Procedures

NUMBER TITLE REVISION

SO123-XV-5.3 Maintenance Rule Program 11

Nuclear Notifications

NUMBER

200457220 200463358 200458378 200704606 200457220

200669151 200695875 200696832 200692595

Maintenance Orders

NUMBER

800321529 800321436 800410821 800318576

Miscellaneous

NUMBER TITLE REVISION /

DATE

3rd Quarter SONGS System Health Reports 0

2009

AR 030500466 SONGS Operational Experience Reviews May 9, 2003

EDGS SONGS 3rd Quarter EDGS System Health Report September 21,

2009

MJ7058 Personnel Qualification Standard - Advanced Soldering 2

MT7058 Lesson Plan - Advanced Soldering 2

A-10 Attachment

Section 1R13: Maintenance Risk Assessment and Emergent Work Controls

Procedures

NUMBER TITLE REVISION

SO123-I-1.13 NUREG 0612 Cranes, Rigging and Lifting Controls 17

SO23-1-3.3 Reactor Vessel Head Removal and Storage 13

SO123-1-7.14 Maintenance and Inspection of Cranes 10

Nuclear Notifications

NUMBER

200394201 200628904 200648805 200648807 200641130

200615912 200701778

Maintenance Orders

NUMBER

WCA 700002477 NMO 800251432 NECP 800175646 NECP 800072640

NECP 800130487

Drawings

NUMBER TITLE REVISION

23156-3 Containment Interior Structure Inserts 0

21015 Underground Utilities Protection Plan and Sections 8

25211-002 Unit 2 Service Crane/Runway Erection and Load Drop 0

Zones

716029 SH1 Unit 2 Safe Load Path 4

Calculations

NUMBER TITLE REVISION

A-11 Attachment

Section 1R13: Maintenance Risk Assessment and Emergent Work Controls

25221-000-COC- Outside Lift System and Erection and Collapse Load Drop 0

7100-00011 Effects

Miscellaneous

NUMBER TITLE REVISION

DID 4a Defense in Depth Sheet 4a 1

R2C16 Probabilistic Risk Assessment Group Recommendations 0

Risk Matrix Analysis- 480V transformer addition project 0

PMP

WCCP 15000 Reactor Head Lift 0

Section 1R15: Operability Evaluations

Procedures

NUMBER TITLE REVISION

SO123-XV-5 Nonconforming Materials, Parts, or Components 19

SO123-XV-52 Functionality Assessments and Operability Determinations 13

SO123-0-A3 Procedure Use 8

SO23-3-2.11.1 SFP Level Change and Purification Crosstie Operations 14

SO23-13-2 Shutdown from Outside the Control Room 12

SO123-XV-52 Functionality Assessments and Operability Determination 14

SO23-3-3.23 Diesel Generator Monthly and Semi-Annual Testing 43

SO123-XX-19 Operational Decision Making 4

Nuclear Notifications

A-12 Attachment

NUMBER

200645996 200643134 200695732 200692347 200691509

200682817 200689450 200683165 200683974 200689450

200683739 200704606 200457220 200702905 200695875

200696832 200669151 200700917

Drawings

NUMBER TITLE

835878 3000 Amp Jump Assembly

835879 Jump Assemblies 75 to 350 MVA

Calculations

NUMBER TITLE REVISION

J-KJA-012 Diesel Generator Low Lube Oil Level Alarm Setpoint 1

Maintenance Orders

NUMBER

800410821

Section 1R18: Plant Modifications

Procedures

NUMBER TITLE REVISION

P-2902-28 Hydraulic Life Device Load Test 0

P-2902-26 Temporary Handling Device Load Tet 0

Nuclear Notifications

NUMBER

200638659 200634389

A-13 Attachment

Maintenance Orders

NUMBER

NECP 800072651

Drawings

NUMBER TITLE REVISION

SO23-617-3B-D53 Temporary Handling Device 0

SO23-617-3B-D563 Load Test Hydraulic Lifter and Details 0

Calculations

NUMBER TITLE REVISION /

DATE

SO23-617-1-C995 Evaluation for Replacement Steam Generator (RSG) 0

Pedestal Skirt Bolt Hole Enlargement and Stud Deletion

Section 1R19: Postmaintenance Testing

Procedures

NUMBER TITLE REVISION

SO23-6-32 Electrical Bus Outages 16

SO23-6-2 Transferring of 4KV Buses 15

SO23-3-3.27.2 Weekly Electrical Bus Surveillance 19

SO23-3-3.23 Diesel Generator Monthly and Semi-Annual Testing 43

Nuclear Notifications

NUMBER

200638791 200657834 200402124 200695875 200696832

200669151 200700917

Maintenance Orders

A-14 Attachment

NUMBER

800397782 WCD 30003055 WCA 70002397 800256628 800410821

800429930 800430174 800130487 800404685

Drawings

NUMBER TITLE REVISION

30162 480 Volt Motor Control Center 2BY 35

30216 Elementary Diagram Electrical Auxiliary 4.16KV Bus 2A06 21

Tie Breaker

30299 Sheet 2 Elementary Diagram Electrical Auxiliary 4.16KV Bus 2A06 20

Metering

30220 Sheet 1 Elementary Diagram Electrical Auxiliary 4.16KV Bus 2A06 15

Metering

Miscellaneous

NUMBER TITLE DATE

Letter From Impact of U2 LOVS Relay Work on U3 Safety Busses December 4,

Gary Segich to 2009

Lou Bosch

Section 1R20: Refueling and Other Outage Activities

Procedures

NUMBER TITLE REVISION /

DATE

SO23-X-7 Refueling Operations 19

SO123-I-1.43 Maintenance Human Performance Application 9

25221-PP-63 Tendon Replacement Methodology Demonstration 0

Program

A-15 Attachment

Section 1R20: Refueling and Other Outage Activities

SO23-3-3.23 AC Sources Verification (Modes 5, 6, and Defueled) 41

Attachment 8

SO23-3-1.7 Aligning the Oil Lift Pump(s) and/or ARRD Pump(s) 35

Power Supplies

P-2502-30 Runway and Outside Lift System Installation and

Removal Program

Specification 240 Steam Generator Skirt Flange Bolts- Preload Evaluation September 30,

1980

SO123-XV-23.1 Housekeeping 4

SGRPP-SO123-G-1 Event Response Plan 1

SO23-X-7.2 Nuclear Fuel Management - Spent Fuel Pool 18

SO23-5-1.8.1 Shutdown Nuclear Safety 23

SO23-I-6.155 Containment Equipment Access Hatch Operation 9

Nuclear Notifications

NUMBER

200616238 200637174 200626409 2000633500 200616724

200620113 200611066 200606500 200613762 200619631

Maintenance Orders

NUMBER

800257416 800221379 800280086 800229724 800279989

800221369 800251355 800251357 800251354 800251435

800257416 8000313756

A-16 Attachment

Drawings

NUMBER TITLE REVISION

23056 Containment Structure Wall Liner and Installation 0

SO23-915-45 Steam Generator Support Installation 5

41276 Area CA10 drain 50' Elevation plans 8

Work Control Activities/Documents

NUMBER

30003180 30003055 70001551 30002002 30002007

700002478 30002398 30001921 30003180

Calculations

NUMBER TITLE REVISION /

DATE

25221-PP-05 Bechtel Project Plan Containment Opening Plan 2

M-120.09 Flooding Analysis April 20, 1977

Miscellaneous

NUMBER TITLE REVISION

WPIR WCN 25221- Chipping and Cutting for the Containment Construction Hole 0

002-CON-3050-

20114

WPIR WCN 25221- Preassembly Erection and Disassembly of inside runway

002-COP-0058-

00106

WPIR WCN 25221- Steam Generator Replacement 89 Whip Restraint Removal

002-MOP-7057-

0882

Section 1R22: Surveillance Testing

A-17 Attachment

Section 1R22: Surveillance Testing

Procedures

NUMBER TITLE REVISION

SO23-5-1.1 Heat Treating the Circulating Water System 23

SO23-13-10 Loss of Condenser Vacuum 8

SO23-V-3.4 Engineering Procedure Inservice tests 18

SO23-3-3.60.6 Surveillance Operating Instruction Inservice test 16

SO23-3-3.51 Containment Penetration Leak Rate Testing 7

SO23-3-3.51.8 Containment Penetration Leak Rate Testing Air System 9

Penetrations

SO23-3-3.23 Diesel Generator Monthly Testing 41

SO123-0-A4 Diesel Generator Starts 12

SO23-3-3.60.7 Containment Spray Pump 3MP-012 Group B Inservice Test 12

2JQ203B Local Leak Rate Testing (LLRT) Qualification Guide 1

2JQ101G Inservice Pump Testing Qualification Guide 1

Nuclear Notifications

NUMBER

200598566 200615026 200616518

Drawings

NUMBER TITLE REVISION

41061 AFW 2P504 Pump Curve 2

Miscellaneous

NUMBER TITLE DATE

Penetration 21 Test Data Sheet October 8, 2009

A-18 Attachment

Section 1EP1: Exercise Evaluation

Procedures

NUMBER TITLE REVISION

SO123-VIII-1 Recognition and Classification of Emergencies 28

SO123-VIII-10 Emergency Coordinator Duties 25-1

SO123-VIII-10.1 Station Emergency Director Duties 18-1

SO123-VIII-10.2 Corporate Emergency Director Duties 14-1

SO123-VIII-10.3 Protective Action Recommendations 12

SO123-VIII-30.3 OSC Operations Coordinator Duties 6

SO123-VIII-30.7 Emergency Notifications 11

SO123-VIII-40.100 Dose Assessment 13

Section 1EP6: Drill Evaluation

Miscellaneous

NUMBER TITLE REVISION

NEI 99-02 Regulatory Assessment Performance Indicator Guideline 5

Section 2OS1: Access Controls to Radiologically Significant Areas

AUDITS, SELF-ASSESSMENTS, AND SURVEILLANCES

TITLE

HPD U2C16 Refuel Outage 30 Day Self-Assessment

Procedures

A-19 Attachment

NUMBER TITLE REVISION

SO123-VII-20.6 External Occupational Exposure Monitoring 9

SO123-VII-20.9 Radiological Surveys 9

SO123-VII- Health Physics Pre-Job Briefings/Pre-job Meetings 5

20.10.2

SO123-VII- Access Control Program 12

20.11

SO123-VII- Radiological Posting 10

20.11.1

Nuclear Notifications

NUMBER

200530881 200596501 200623393 200625730

Radiation Work Permits

NUMBER TITLE

800211520 Perform ISI Inspections in U2C16 outage

800211882 Regenerative Heat Exchanger

A0216090013 2SGRP - RCS Piping Work

A0216090015 2SGRP - RCS Pipe End Decon

Section 2OS2: ALARA Planning and Controls

Procedures

NUMBER TITLE REVISION

SO123-VII- Radiological Work Planning and Controls 14

20.10

A-20 Attachment

Section 2OS2: ALARA Planning and Controls

SO123-VII-20.4 ALARA Program

Miscellaneous

NUMBER TITLE REVISION

R2C16 Outage ALARA Plan 0

Section 4OA1: Performance Indicator Verification

Procedures

NUMBER TITLE REVISION

SO123-VIII-1 Recognition and Classification of Emergencies 26, 27, 28

SO123-VIII-10.3 Protective Action Recommendations 11, 12

SO123-VII-30.7 Emergency Notifications 10, 11

Drills and Exercises

NUMBER TITLE DATE

0905 Emergency Plan Drill August 19, 2009

0904 ERO Restructure June 24, 2009

0903 Environmental April 8, 2009

0902 Assembly March 17, 2009

0901 Backshift January 6-12,

2009

0812 Contaminated Injury November 19,

2008

A-21 Attachment

Section 4OA1: Performance Indicator Verification

0806 Environmental October 8, 2008

0805 INPO Visit September 17,

2008

0804 Proficiency August 27, 2008

0803 Hostile Action Drill May 7, 2008

0802 Hostile Action Table Top April 23, 2008

0801 Mini-Drill April 2, 2008

0702 Emergency Plan Exercise April 18, 2007

0701 Emergency Plan Drill March 14, 2007

0502 Emergency Plan Exercise April 13, 2005

0501 Emergency Plan Drill March 9, 2005

Miscellaneous

NUMBER TITLE REVISION

San Onofre Nuclear Generating Station Emergency Plan 25, 26

SA-1 Self Assessment Program 5

VIII-0.202 Assignment of Emergency Response Personnel 10

XII-2.7 Reporting of Quality Trends 3-2

XV-50 Corrective Action Program 12

XV-50.CAP-2 SONGS Nuclear Notification Screening 2

A-22 Attachment

Section 4OA1: Performance Indicator Verification

XV-50.CAP-3 Corrective Action Program Evaluations and Action Plans 1

SO123-XXI-1.11.3 Emergency Plan Training Program Description 20, 21

Section 4OA2: Identification and Resolution of Problems

Procedures

NUMBER TITLE REVISION /

DATE

SO123-0-A1 Conduct of Operations 26

SO23-XVII-3.2.1 Class 2 System Leakage Test of the Chemical and 4

Volume Control System

Nuclear Notifications

NUMBER

200685073 200614441 200683697 200683767 200683165

200682817 200687365 200120199 200129036 200175511

200007225 200211509 200231399 200252142 200253424

200278159 200226143 200278221 200278222 200027824

200278227 200336666 200345873 200352006 200356782

200357504 200370464 200417017 200444208 200444284

200456915 200459256 200462583 200498500 200501123

200535198 200544102 200552330 200597585

Action requests

A-23 Attachment

NUMBER

011200984 950600074

Drawings

S3-1219-ML-057 From RWT T006 to Line 007 10

Maintenance Orders

800415935 800415909 800416417

Miscellaneous

NUMBER TITLE REVISION /

DATE

Document 90463 Unit 2 and 3 Schedule 10, Stainless Steel Piping Inspection 0

and Repair Plan

RCE 92-018 Corrosion of Stainless Steel Piping in the FFCPD System June 19,

Sluice Water Inlet Line 1992

Failure Analysis Failure Analysis of BAMU Line Cracking February 1,

Report 96-001 1996

Section 4OA3: Event Follow-Up

Procedures

NUMBER TITLE REVISION / DATE

LER 05000361/2007-005-00 Loose Electrical Connection Results in October 16, 2008

Inoperable Pump Room Cooler

LER 05000361/2008-005-00 Missed SR for Mode Change July 30, 2008

LER 05000361;05000362/2008- Failed to Comply with Completion Time November 14,

007-00 for SR 3.8.1.1 2008

SO123-0-A4 Configuration Control 12

A-24 Attachment

Section 4OA3: Event Follow-Up

SO123-XV-HU-1 Human Performance Program 3

SO123-0-A1 Conduct of Operations 25

SO23-6-33 Ground Isolation 6

SO23-5.1.1 Heat Treating the Circulating Water 22

System

SO23-13-10 Loss of Condenser Vacuum 8

OSM-6 Operations Department Human 8

Performance Tools

SO123-0-A1 Conduct of Operations 24

SO123-XV-HU-1 Human Performance Program 2

OSM-12 Operator Fundamentals 9

SO123-XV-1.41 Control of Ignition Sources 13

SO23-2-8 Saltwater Cooling System Operation 32

SO23-13-7 Loss of Cooling Water/Saltwater Cooling 14

Nuclear Notifications

NUMBER

200638837 200638791 200638786 200648875 200626763

200638641 200636533 200100730 200666537 20067114

A-25 Attachment

Section 4OA3: Event Follow-Up

200704617 200580999 200718204 200572373 200601793

200602881 200619437 200602213 200614395 200618783

200602881 200617708

Action Requests

NUMBER

070300033

Miscellaneous

NUMBER TITLE

Personnel Statements

Control Room Logs

45564 Event Log

A-26 Attachment