ML060460035

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IR 05000275-05-005, 05000323-05-005; 10/1-12/31/05; Diablo Canyon Units 1 & 2; Personnel Performance Related to Nonroutine Plant Evolutions & Events, & Problem Identification & Resolution, Access Control to Radiologically Significant Areas,
ML060460035
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 02/14/2006
From: William Jones
NRC/RGN-IV/DRP/RPB-B
To: Keenan J
Pacific Gas & Electric Co
References
IR-05-005
Download: ML060460035 (60)


See also: IR 05000275/2005005

Text

February 14, 2006

John S. Keenan, Chief Nuclear Officer

Pacific Gas and Electric Company

Mail Code B32

P.O. Box 770000

San Francisco, California 94177-0001

SUBJECT: DIABLO CANYON POWER PLANT - NRC INTEGRATED INSPECTION

REPORT 05000275/2005005 AND 05000323/2005005

Dear Mr. Keenan:

On December 31, 2005, the U.S. Nuclear Regulatory Commission completed an inspection at

your Diablo Canyon Power Plant, Units 1 and 2, facility. The enclosed integrated report

documents the inspection findings that were discussed on January 12, 2006, with Mr. David

Oatley and members of your staff.

This inspection examined activities conducted under your licenses as they relate to safety and

compliance with the Commission's rules and regulations, and with the conditions of your

licenses. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel.

There were two NRC-identified findings and two self-revealing findings of very low safety

significance (Green) identified in this report. These findings involved violations of NRC

requirements. In addition, licensee-identified violations which were determined to be of very low

safety significance are listed in the report. One additional NRC-identified finding was reviewed

under the NRC traditional enforcement process and determined to be a Severity Level IV

violation of NRC requirements. Because of their very low risk significance and because they

are entered into your corrective action program, the NRC is treating these five findings as

noncited violations (NCVs) consistent with Section VI.A of the NRC Enforcement Policy. If you

contest any NCV in this report, you should provide a response within 30 days of the date of this

inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611 Ryan Plaza Drive,

Suite 400, Arlington, Texas 76011-4005; the Director, Office of Enforcement, U.S. Nuclear

Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the

Diablo Canyon Power Plant.

Pacific Gas and Electric Company -2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document

system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-

rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

William B. Jones, Chief

Project Branch B

Division of Reactor Projects

Dockets: 50-275

50-323

Licenses: DPR-80

DPR-82

Enclosure:

Inspection Report 05000275/2005005

and 05000323/2005005

w/attachment: Supplemental Information

cc w/enclosure:

David H. Oatley, Acting

Chief Nuclear Officer

Diablo Canyon Power Plant

P.O. Box 56

Avila Beach, CA 93424

Donna Jacobs

Vice President, Nuclear Services

Diablo Canyon Power Plant

P.O. Box 56

Avila Beach, CA 93424

James R. Becker, Vice President

Diablo Canyon Operations and

Station Director, Pacific Gas and

Electric Company

Diablo Canyon Power Plant

P.O. Box 3

Avila Beach, CA 93424

Pacific Gas and Electric Company -3-

Sierra Club San Lucia Chapter

ATTN: Andrew Christie

P.O. Box 15755

San Luis Obispo, CA 93406

Nancy Culver

San Luis Obispo Mothers for Peace

P.O. Box 164

Pismo Beach, CA 93448

Chairman

San Luis Obispo County Board of

Supervisors

Room 370

County Government Center

San Luis Obispo, CA 93408

Truman Burns\Robert Kinosian

California Public Utilities Commission

505 Van Ness Ave., Rm. 4102

San Francisco, CA 94102-3298

Diablo Canyon Independent Safety Committee

Robert R. Wellington, Esq.

Legal Counsel

857 Cass Street, Suite D

Monterey, CA 93940

Ed Bailey, Chief

Radiologic Health Branch

State Department of Health Services

P.O. Box 997414 (MS 7610)

Sacramento, CA 95899-7414

Richard F. Locke, Esq.

Pacific Gas and Electric Company

P.O. Box 7442

San Francisco, CA 94120

City Editor

The Tribune

3825 South Higuera Street

P.O. Box 112

San Luis Obispo, CA 93406-0112

Pacific Gas and Electric Company -4-

James D. Boyd, Commissioner

California Energy Commission

1516 Ninth Street (MS 34)

Sacramento, CA 95814

Jennifer Tang

Field Representative

United States Senator Barbara Boxer

1700 Montgomery Street, Suite 240

San Francisco, CA 94111

Chief, Radiological Emergency

Preparedness Section

Oakland Field Office

Chemical and Nuclear Preparedness

and Protection Division

Department of Homeland Security

1111 Broadway, Suite 1200

Oakland, CA 94607-4052

Pacific Gas and Electric Company -5-

Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

DRS Director (DDC)

DRS Deputy Director (RJC1)

Senior Resident Inspector (TWJ)

Branch Chief, DRP/B (WBJ)

Senior Project Engineer, DRP/E (RAK1)

Team Leader, DRP/TSS (RLN1)

RITS Coordinator (KEG)

DRS STA (DAP)

V. Dricks, PAO (VLD)

J. Dixon-Herrity, OEDO RIV Coordinator (JLD)

ROPreports

DC Site Secretary (AWC1)

W. A. Maier, RSLO (WAM)

SUNSI Review Completed: _wbj___ADAMS: : Yes G No Initials: __wbj____

Publicly Available G Non-Publicly Available G Sensitive  : Non-Sensitive

R:\_REACTORS\_DC\2005\DC2005-05RP-TWJ.wpd

RIV:RI:DRP/B SRI:DRP/B C:DRS/PSB C:DRS/OB C:DRS/PEB

TAMcConnell TWJackson MPShannon ATGody LJSmith

E - WBJones E - WBJones /RA/ /RA/ GDReplogle for

2/10/06 2/10/06 2/13/06 2/13/06 2/13/06

C:DRS/EB C:DRP/B

JAClark WBJones

/RA/ /RA/

2/13/06 2/14/06

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

ENCLOSURE

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Dockets: 50-275, 50-323

Licenses: DPR-80, DPR-82

Report: 05000275/2005005

05000323/2005005

Licensee: Pacific Gas and Electric Company (PG&E)

Facility: Diablo Canyon Power Plant, Units 1 and 2

Location: 7 1/2 miles NW of Avila Beach

Avila Beach, California

Dates: October 1 through December 31, 2005

Inspectors: T. Jackson, Senior Resident Inspector

T. McConnell, Resident Inspector

R. Lantz, Senior Emergency Preparedness Inspector

R. Kopriva, Senior Project Engineer

L. Ricketson, PE, Senior Health Physicist

J. Adams, Reactor Inspector

L. Ellershaw, PE, Consultant

Approved By: W. B. Jones, Chief, Projects Branch B

Division of Reactor Projects

-1- Enclosure

TABLE OF CONTENTS

PAGE

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

REACTOR SAFETY

1R01 Adverse Weather . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8

1R04 Equipment Alignments . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8

1R05 Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

1R06 Flood Protection Measures . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

1R07 Heat Sink Performance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

1R08 Inservice Inspection Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11

1R11 Licensed Operator Requalification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

1R12 Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

1R13 Maintenance Risk Assessments and Emergent Work Control . . . . . . . . . . . . . 18

1R14 Personnel Performance Related to Nonroutine Plant Evolutions and Events . 19

1R15 Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

1R19 Postmaintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 25

1R20 Refueling and Outage Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

1R22 Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

1EP2 Alert Notification System Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28

1EP3 Emergency Response Organization Augmentation Testing . . . . . . . . . . . . . . 29

1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies . . . . . 29

1EP6 Emergency Preparedness Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 30

RADIATION SAFETY

2OS1 Access Control To Radiologically Significant Areas . . . . . . . . . . . . . . . . . . . . 30

OTHER ACTIVITIES

4OA1 Performance Indicator Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 33

4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . 36

4OA3 Event Follow-up . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 42

4OA5 Other . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 45

4OA6 Management Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 46

4OA7 Licensee-identified Violations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 42

ATTACHMENT: SUPPLEMENTAL INFORMATION

Key Points of Contact . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

List of Items Opened, Closed, and Discussed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

List of Documents Reviewed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-2

List of Acronyms Used . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-9

-2- Enclosure

SUMMARY OF FINDINGS

IR 05000275/2005-005, 05000323/2005-005; 10/1/05 - 12/31/05; Diablo Canyon Power Plant

Units 1 and 2; Personnel Performance Related to Nonroutine Plant Evolutions and Events, and

Problem Identification and Resolution, Access Control to Radiologically Significant Areas, and

Performance Indicator Verification.

This report covered a 13-week period of inspection by resident inspectors and announced

inspections in the areas of radiation protection and in-service inspections. Two self-revealing

and two NRC- identified, Green, noncited violations were identified. Additionally, a Severity

Level IV violation was identified. The significance of most findings is indicated by their color

(Green, White, Yellow, or Red) using Inspection Manual Chapter 0609 Significance

Determination Process. Findings for which the Significance Determination Process does not

apply may be Green or be assigned a severity level after NRC management review. The

NRCs program for overseeing the safe operation of commercial nuclear power reactors is

described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

for the failure of maintenance personnel to adequately assess and manage the

risk associated with maintenance on Startup Transformer 1-1. On November 19,

2005, when maintenance personnel were performing work on Startup

Transformer 1-1, they failed to conduct a circuit isolation plan which was a risk

management action required by Procedures AD7.DC8, Work Control,

Revision 20 and MA1.DC11, Risk Assessment, Revision 5A. The circuit

isolation plan would have provided an opportunity to identify the potential of

disrupting startup power to Unit 2, which occurred as a result of the maintenance

activities. This issue was entered into Pacific Gas and Electric

Companys corrective action program as Action Request A0652421.

The finding was greater than minor because it is related to Inspection Manual

Chapter 0612, Appendix B, Section 3(5)(I), in that maintenance personnel failed

to fully implement Procedures AD7.DC8 and MA1.DC11, which called for a

circuit isolation plan for medium- to high-risk maintenance activities as a risk

management action. The finding affected the Mitigating Systems Cornerstone.

Using Inspection Manual Chapter 0609, Appendix K, Maintenance Risk

Assessment and Risk Management Significance Determination Process,

Flowchart 2 - Assessment of Risk Management Actions, the incremental core

damage probability was less than 1E-6 and the incremental large early release

frequency was less than 1E-7. The finding was assessed as having very low

safety significance. The cause of the finding is related to the cross-cutting

element of human performance in that maintenance personnel failed to follow

procedures (Section 1R14).

-3- Enclosure

identified for the failure of operations personnel to properly implement

Procedure OP B-3B:I, Accumulators - Fill and Pressurize, Revision 23. On

November 27, 2005, operators failed to correctly align valves according to

Procedure OP B-3B:I in order to fill Safety Injection Accumulator 1-3. As a

result, the safety injection pumps injected into the reactor coolant system

causing the pressurizer heatup rate to be exceeded and contributing to the

safety injection discharge header pressurization due to perturbation of check

Valve SI-1-8948B. This violation was entered into Pacific Gas and Electric

Companys corrective action program as Action Request A0653564.

The finding is greater than minor because it is associated with the Mitigating

System Cornerstone attribute of configuration control and affects the associated

cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

Using the Inspection Manual Chapter 0609, "Significance Determination

Process," Appendix G, Checklist 4, the finding did not require quantitative

screening. Therefore, the finding was assessed as having very low safety

significance. The cause of the finding is related to the crosscutting element of

human performance in that operations personnel did not follow procedures

(Section 1R14).

was identified for the failure to promptly correct emergency core cooling system

check valve back-leakage. Since 2000, Units 1 and 2 have experienced

emergency core cooling system check valve back-leakage. Pacific Gas and

Electric Company has failed to adequately take into consideration industry

experience and provide for timely corrective actions regarding emergency core

cooling system check valve back-leakage and its potential to cause gas-binding

of emergency core cooling system pumps and/or water hammer of emergency

core cooling system piping. This issue was entered into Pacific Gas and Electric

Companys corrective action program as Action Requests A0526037

and A0610421.

The finding is greater than minor because it is associated with the Mitigating

Systems Cornerstone attribute of equipment performance and affects the

associated cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. Using Inspection Manual Chapter 0609, Significance

Determination Process, Phase 1 Worksheet, the finding is determined to have

very low safety significance because it did not represent an actual loss of safety

function, represent an actual loss of safety function for a single train for greater

than the Technical Specification allowed outage time, or screen as potentially

risk significant due to seismic, fire, flooding, or severe weather initiating events.

The cause of the finding is related to the crosscutting element of problem

-4- Enclosure

identification and resolution in that Pacific Gas and Electric Company did not

adequately evaluate and implement timely corrective actions to emergency core

cooling system check valve back-leakage (Section 4OA2.2).

Cornerstone: Emergency Preparedness

because Pacific Gas and Electric Company failed to provide complete and

accurate information in a submittal of data for the emergency preparedness drill

and exercise performance indicator. Specifically, Pacific Gas and Electric

Company staff failed to identify three missed opportunities for emergency

notification accuracy during the second calendar quarter of 2005. Pacific Gas

and Electric Company took prompt action to correct the second quarter data,

which resulted in the drill and exercise performance indicator color to cross from

GREEN to WHITE. Pacific Gas and Electric Company also initiated a

100 percent review of the second and third quarter drill and exercise

performance indicator data and discovered one additional administrative error in

the third quarter performance indicator data, which had been previously

evaluated, but not yet reported to the NRC. Pacific Gas and Electric Company

had previously initiated a root cause evaluation in its corrective action program to

determine the reason for the declining indicator and, subsequently, initiated

another root cause evaluation to determine the reason for the failure to

adequately evaluate and report the performance indicator data. The finding also

had human performance crosscutting aspects in that the reviews that were

performed were not adequate to identify the actual failures that had occurred.

Because this issue affected the NRCs ability to perform its regulatory function, it

was evaluated using the traditional enforcement process. Supplement 7,

Section D.3, of the NRC Enforcement Policy describes this finding as a Severity

Level IV violation. The issue is significant because it indicates a declining trend

in the attention to detail shown by senior licensed operators in performing

emergency notifications to the state and local authorities. This issue is

documented in Pacific Gas and Electric Company's corrective action program as

Nonconformance Report N0002200 (Section 4OA1).

Cornerstone: Occupational Radiation Safety

  • Green. The inspectors identified an noncited violation of 10 CFR 20.1902 for a

failure of Pacific Gas and Electric Company to post a radiation area.

Specifically, Pacific Gas and Electric Company did not post an area within

Vault 26 in which the radiation dose rates were approximately 30 millirem per

hour at 30 centimeters from the surfaces of radioactive material storage

containers. The finding was entered into Pacific Gas and Electric Companys

corrective action program as Action Request A0652226 and planned corrective

action were still being evaluated. The finding had crosscutting aspects in the

area problem identification and resolution (corrective actions), in that a similar

violation was previously identified in Inspection Report 050000275; 323/2002004.

-5- Enclosure

The finding was more than minor because it was associated with one of the

cornerstone attributes (exposure control and monitoring) and the finding affected

the Occupational Radiation Safety Cornerstone objective, in that uninformed

workers could unknowingly accrue additional radiation dose. The inspector

determined that the finding had no more than very low safety significance

because: (1) it did not involve ALARA planning and controls, (2) there was no

personnel overexposure, (3) there was no substantial potential for personnel

overexposure, and (4) the finding did not compromise Pacific Gas and Electric

Companys ability to assess dose (Section 2OS1).

B. Licensee-Identified Violations

Violations of very low safety significance, which have been identified by Pacific Gas and

Electric Company have been reviewed by the inspectors. Corrective actions taken or

planned by Pacific Gas and Electric Company have been entered into their corrective

action program. These violations and corrective actions are listed in Section 4OA7 of

this report.

-6- Enclosure

REPORT DETAILS

Summary of Plant Status

Diablo Canyon Power Plant Unit 1 began this inspection period at 100 percent power. On

October 15, 2005, Unit 1 was curtailed to 93 percent power due to the loss of hydrazine

injection into the secondary feedwater system. Unit 1 returned to 100 percent power following

the restoration of hydrazine on the same day. On October 22, Unit 1 was curtailed to

23 percent power as a precaution due to high storm ocean swells.

On October 23, 2005, operators commenced a Unit 1 reactor shutdown for Refueling

Outage 1R13 and entered Mode 3 (Hot Standby). Operators initiated a plant cooldown and

entered Mode 4 (Hot Shutdown) on October 23 and Mode 5 (Cold Shutdown) on October 24.

On October 28, Unit 1 entered Mode 6 (Refueling) when maintenance personnel de-tensioned

the reactor vessel head. Operators commenced core offload on October 30 and completed

core offload on November 1. Unit 1 remained de-fueled until November 17 when Unit 1 entered

Mode 6 as a result of operators reloading fuel into the reactor vessel. Unit 1 entered Mode 5 on

November 22 when maintenance personnel tensioned the reactor vessel head. Operators

began increasing reactor coolant temperature, and Unit 1 entered Mode 4 on November 26.

Operators continued to increase reactor coolant temperature, and Unit 1 entered Mode 3 on

November 28. On November 29, operators commenced a reactor startup, and Unit 1 reached

Mode 2 (Startup). Operators continued to increase reactor power, and Unit 1 entered Mode 1

(Power Operations) on December 2. On December 3, the Unit 1 main generator was paralleled

to the grid; ending Refueling Outage 1R13. Unit 1 reached 100 percent power on December 8.

On December 20, 2005, Unit 1 was curtailed to 25 percent power as a precaution due to high

ocean swells. Unit 1 was returned to 100 percent power on December 21. Unit 1 remained at

100 percent power for the duration of the inspection period.

Diablo Canyon Power Plant Unit 2 began this inspection period at 100 percent power. On

October 1, 2005, Unit 2 was curtailed to 87 percent power to support grid maintenance.

Following completion of this maintenance activity, Unit 2 was returned to 100 percent power on

October 2. On October 22, Unit 2 was curtailed to 23 percent power as a precaution due to

high ocean swells. Unit 2 was returned to 100 percent power on October 24. On November 9,

Unit 2 was curtailed to approximately 99 percent power for replacement of a feedwater heater

valve. Following valve replacement, Unit 2 was returned to 100 percent power on

November 12. On December 20, Unit 2 was curtailed to 25 percent power as a precaution due

to high ocean swells. Unit 2 was returned to 100 percent power on December 21. Unit 2

remained at 100 percent power for the duration of the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

-7- Enclosure

1R01 Adverse Weather (71111.01)

a. Inspection Scope

The inspectors completed a review of Pacific Gas and Electric Company's (PG&E)

readiness of seasonal susceptibilities involving extreme low temperatures. The

inspectors: (1) reviewed plant procedures, the Final Safety Analysis Report (FSAR)

Update, and Technical Specifications (TS) to ensure that operator actions defined in

adverse weather procedures maintained the readiness of essential systems; (2) walked

down portions of the one system listed below to ensure that adverse weather protection

features (heat tracing, space heaters, weatherized enclosures, etc.) were sufficient to

support operability, including the ability to perform safe shutdown functions; (3)

evaluated operator staffing levels to ensure PG&E could maintain the readiness of

essential systems required by plant procedures; and (4) reviewed thecorrective action

program to determine if PG&E identified and corrected problems related to adverse

weather conditions.

  • December 22, 2005: Units 1 and 2, Vital Batteries

Documents reviewed by the inspectors included:

  • Procedure Action Request (AR) PK15-09, Electrical Rooms Temp Monitor,

Revision 26

  • Design Criteria Memorandum S-67, 125 and 250V DC System, Revision 2

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignments (71111.04)

Partial System Walkdowns

a. Inspection Scope

The inspectors: (1) walked down portions of the below listed risk-important system and

reviewed plant procedures and documents to verify that critical portions of the selected

systems were correctly aligned; and (2) compared deficiencies identified during the walk

down to the FSAR Update and CAP to ensure problems were being identified and

corrected.

  • October 7, 2005: Unit 1, Auxiliary Saltwater Pump 1-1

-8- Enclosure

Documents reviewed by the inspectors included:

  • Drawing 106717, Saltwater, Sheet 7, Revision 132
  • Drawing 106717, Saltwater, Sheet 7A, Revision 138

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

.1 Quarterly Inspection

a. Inspection Scope

The inspectors walked down the two below listed plant areas to assess the material

condition of active and passive fire protection features and their operational lineup and

readiness. The inspectors: (1) verified that transient combustibles and hot work

activities were controlled in accordance with plant procedures; (2) observed the

condition of fire detection devices to verify they remained functional; (3) observed fire

suppression systems to verify they remained functional and that access to manual

actuators was unobstructed; (4) verified that fire extinguishers and hose stations were

provided at their designated locations and that they were in a satisfactory condition;

(5) verified that passive fire protection features (electrical raceway barriers, fire doors,

fire dampers, steel fire proofing, penetration seals, and oil collection systems) were in a

satisfactory material condition; (6) verified that adequate compensatory measures were

established for degraded or inoperable fire protection features and that the

compensatory measures were commensurate with the significance of the deficiency;

and (7) reviewed the FSAR Update to determine if PG&E identified and corrected fire

protection problems.

  • November 7, 2005: Unit 1, Containment Fire Zones 1A, 1B, and 1C
  • November 8, 2005: Unit 1, 154 foot Auxiliary Building, Detection Zone A-13

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed two samples.

b. Findings

No findings of significance were identified.

-9- Enclosure

1R06 Flood Protection Measures (71111.06)

Annual External Flooding

a. Inspection Scope

The inspectors: (1) reviewed the FSAR Update, the flooding analysis, and plant

procedures to assess seasonal susceptibilities involving external flooding; (2) reviewed

the FSAR Update and CAP to determine if PG&E identified and corrected flooding

problems; (3) inspected underground bunkers/manholes to verify the adequacy of

(a) sump pumps, (b) level alarm circuits, (c) cable splices subject to submergence, and

(d) drainage for bunkers/manholes; (4) verified that operator actions for coping with

flooding can reasonably achieve the desired outcomes; and (5) walked down the one

below listed area to verify the adequacy of: (a) equipment seals located below the

floodline, (b) floor and wall penetration seals, (c) watertight door seals, (d) common

drain lines and sumps, (e) sump pumps, level alarms, and control circuits, and

(f) temporary or removable flood barriers.

  • December 28, 2005: Units 1 and 2, Turbine Building Louvers

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance (71111.07)

a. Inspection Scope

The inspectors reviewed PG&Es programs, verified performance against industry

standards, and reviewed critical operating parameters and maintenance records for

Component Cooling Water Heat Exchangers 1-1 and 1-2. The inspectors verified that :

(1) performance tests were satisfactorily conducted for heat exchangers/heat sinks and

reviewed for problems or errors; (2) PG&E utilized the periodic maintenance method

outlined in EPRI NP-7552, Heat Exchanger Performance Monitoring Guidelines;

(3) PG&E properly utilized biofouling controls; (4) PG&Es heat exchanger inspections

adequately assessed the state of cleanliness of their tubes, and (5) the heat exchanger

was correctly categorized under the Maintenance Rule.

Documents reviewed by the inspectors included Procedure PEP M-234, CCW Heat

Exchanger Performance Test, Revision 9.

The inspectors completed one sample.

-10- Enclosure

b. Findings

No findings of significance were identified.

1R08 Inservice Inspection Activities (71111.08)

Inspection Procedure 71111.08 requires a minimum sample size of four (as identified in

Sections 02.01, 02.02, 02.03, and 02.04).

02.01: Performance of Nondestructive Examination Activities Other Than Steam Generator

Tube Inspections, Pressurized Water Reactor Vessel Upper Head Penetration

Inspections, Boric Acid Corrosion Control

a. Inspection Scope

The inspection procedure requires the review of nondestructive examination activities

consisting of two or three different types (i.e., volumetric, surface, or visual). The

inspectors observed the performance of ultrasonic examinations (volumetric) on eight

reactor vessel upper head penetration nozzles and radiographic examinations

(volumetric) on two emergency core cooling system pipe welds. In addition, the

inspectors observed three liquid penetrant examinations (surface) performed on residual

heat removal system components and reviewed liquid penetrant reports of two

examinations performed on emergency core cooling system pipe welds. The table

below identifies the above examinations, which were conducted using three methods

and two different examination types.

Component Identity Examination Examination

Type Method

Reactor Vessel Upper 30,31,33,36,37,43, 57, Volumetric Ultrasonic

Head Penetration and the vent line weld

Nozzles

Emergency Core Welds WIC 1 and WIC 2 Volumetric Radiography

Cooling System

Suction Void Header

Residual Heat 58N-49R (2 each) Surface Liquid Penetrant

Removal System Pipe

Support Lug welds

Residual Heat 58N-52A Surface Liquid Penetrant

Removal System Pipe

Support Bracket

Emergency Core Welds FW 25 and FW 26 Surface Liquid Penetrant

Cooling System Pipe-

To-Elbow welds

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For each of the nondestructive examination activities reviewed, the inspectors verified

that the examinations were performed in accordance with the specific site procedures

and the applicable American Society of Mechanical Engineers Boiler and Pressure

Vessel Code (ASME Code) requirements.

During review of each examination, the inspectors verified that appropriate

nondestructive examination procedures were used, examinations and conditions were

as specified in the procedure, and test instrumentation or equipment was properly

calibrated and within the allowable calibration period. The inspectors also verified the

nondestructive examination certifications of the personnel who performed the above

ultrasonic and radiographic examinations. Finally, the inspectors observed that

indications identified during the ultrasonic and radiographic examinations were

dispositioned in accordance with the ASME qualified nondestructive examination

procedures used to perform the examinations.

In addition to observation of ultrasonic examinations performed on the eight reactor

vessel upper head penetration nozzles identified in the table above, the inspectors

observed portions of the ultrasonic examination data analysis associated with the

following nine nozzle penetrations: 17, 21, 27, 31, 34, 35, 36, 40, and 74.

The inspection procedure requires review of one or two examinations with recordable

indications that were accepted for continued service to ensure that the disposition was

made in accordance with the ASME Code. The inspectors reviewed AR A0650500,

which documented identification of a flaw in the Loop 3 cold leg nozzle-to-safe end Weld

WIB-RC-3-18(SE). The flaw was identified and documented on November 6, 2005,

during an ultrasonic (volumetric) examination. PG&Es contractor (WesDyne

International) performed an indication sizing assessment on November 7, 2005, using

Procedure PDI-ISI-254-SE, Flaw Sizing, Revision 2. The result of the flaw sizing

evaluation, which showed that the flaw was acceptable, supported continued Unit 1

operation. The inspectors verified that the evaluation was performed in accordance with

the 1989 Edition of the ASME Code,Section XI, Tables IWB-3514-2 and IWB-3514-1,

which provide the specific rules for the performance of such evaluations.

One other instance was identified in which an indication was detected during liquid

penetrant (surface) examination of residual heat removal pipe support Bracket 58N-52A.

The 0.2 inch linear indication was evaluated in accordance with ASME Code

requirements and was found to meet the specified acceptance standards. PG&E

personnel documented the size and location of the indication in the liquid penetrant

examination report.

The inspection procedure further requires verification of one to three welds on Class 1

or 2 pressure boundary piping to ensure that the welding process and welding

examinations were performed in accordance with the ASME Code. The inspectors

verified through record review that welding and subsequent examinations performed on

the Class 2 emergency core cooling system suction void header Welds WIC 1, WIC 2,

FW 25, and FW 26 were performed in accordance with Sections V, IX, and XI of the

1989 Edition of the ASME Code. This included review of welding material issue slips to

establish that the appropriate welding materials had been used, verification of welder

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qualifications, verification that the welding procedure specification (WPS-51) had been

properly qualified, and verification that the applicable nondestructive examination

procedures used to perform the examinations had been qualified. The inspectors also

verified that weld filler materials were properly stored and controlled and that proper

administrative controls were being implemented with respect to issuance and return of

weld filler materials.

The inspectors completed one sample under this section.

b. Findings

No findings of significance were identified.

02.02: Reactor Vessel Upper Head Penetration Inspection Activities

The inspection procedure requires this section to be performed after completion of

Temporary Instruction (TI) 2515/150. The TI had not been completed at the time of this

inspection; therefore, this section was not performed.

02.03: Boric Acid Corrosion Control Inspection Activities (Pressurized Water Reactors)

a. Inspection Scope

The inspectors evaluated the implementation of PG&Es boric acid corrosion control

program for monitoring degradation of those systems that could be deleteriously

affected by boric acid corrosion.

The inspection procedure requires review of a sample of boric acid corrosion control

walkdown visual examination activities through either direct observation or record

review. The inspectors reviewed the documentation associated with PG&Es boric acid

corrosion control walkdown as specified in Procedure ER1.ID2, Boric Acid Corrosion

Control Program, Revision 1. Samples of documented visual inspection records and

filmed results of inspections of components and equipment were also reviewed by the

inspectors.

Additionally, the inspectors performed independent observations of piping containing

boric acid during walkdowns of the containment building and the auxiliary building.

The inspection procedure requires verification that visual inspections emphasize

locations where boric acid leaks can cause degradation of safety significant

components. The inspectors verified through direct observation and program/record

review that PG&Es boric acid corrosion control inspection efforts are directed towards

locations where boric acid leaks can cause degradation of safety-related components.

The inspection procedure requires both a review of one to three engineering evaluations

performed for boric acid leaks found on reactor coolant system piping and components,

and one to three corrective actions performed for identified boric acid leaks. The

inspectors reviewed engineering evaluations associated with ARs A0649000, A0649209,

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and A0649215, which addressed boric acid leaks identified on a body-to-bonnet bolted

connection on a valve in the safety injection system and valve packing leaks on valves

in the reactor coolant system and the safety injection system. The evaluations

appropriately addressed the causes and corrective actions. Additionally, the inspectors

reviewed ARs A0649207 and A0649959 that identified minor boric acid leaks that did

not require formal engineering evaluations to effect corrective actions.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

02.04: Steam Generator Tube Inspection Activities

a. Inspection Scope

The inspection procedure specified performance of an assessment of in-situ screening

criteria to assure consistency between assumed nondestructive examination flaw sizing

accuracy and data from the Electric Power Research Institute (EPRI) examination

technique specification sheets. It further specified assessment of appropriateness of

tubes selected for in situ pressure testing, observation of in situ pressure testing, and

review of in situ pressure test results.

By letter dated October 28, 2005, the NRC issued Amendment 182 to Facility Operating

License DPR-80 and Amendment 184 to Facility Operating License DPR-82 for the

Diablo Canyon Power Plant, Units 1 and 2, respectively. These amendments consist of

changes to the TS and allow use of the steam generator tube W* (W-star) alternate

repair criteria for indications in the Westinghouse explosive tube expansion (WEXTEX)

region on a permanent basis. The W* alternate repair criteria allows axial primary stress

corrosion cracking in the WEXTEX region to remain in service provided the indication

remains below the bottom of the WEXTEX transition during the next operating cycle.

The length of the tube required to be inspected within the hot leg tubesheet is referred

to as the W* distance. While implementation of the W* alternate repair criteria

eliminated the current W* in-situ testing program, other requirements for in-situ testing

remain.

At the time of this inspection, no conditions had been identified that warranted in-situ

pressure testing. The inspectors did, however, review PG&Es report, Steam Generator

Degradation Assessment for Diablo Canyon Unit 1 Refueling Outage 1R13,

October 2005, Revision 0, dated October 28, 2005, and compared the in-situ test

screening parameters to the guidelines contained in the EPRI document, In Situ

Pressure Test Guidelines, Revision 2. This review determined that the remaining

screening parameters were consistent with the EPRI guidelines.

In addition, the inspectors reviewed both PG&E site-validated and qualified acquisition

and analysis technique sheets used during this refueling outage and the qualifying EPRI

examination technique specification sheets to verify that the essential variables

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regarding flaw sizing accuracy, tubing, equipment, technique, and analysis had been

identified and qualified through demonstration. The inspector-reviewed acquisition

technique and analysis technique sheets are identified in the Attachment.

The inspection procedure specified comparing the estimated size and number of tube

flaws detected during the current outage against the previous outage operational

assessment predictions to assess the licensees prediction capability. The inspectors

compared the previous outage operational assessment predictions with the flaws

identified thus far during the current steam generator tube inspection effort. Compared

to the projected damage mechanisms identified by PG&E, the number of identified

indications fell within the range of prediction and were quite consistent with predictions.

The number of circular outside diameter stress corrosion cracking flaws, however, was

higher than predicted. Thus, the number of tubes identified for plugging was higher than

expected. As a result, PG&E placed Steam Generators 1-1 and 1-2 in TS C-3 category

based on the total number of defective tubes identified during eddy current testing. The

consequence of entering C-3 category requires an increase in tube sample size for eddy

current examination, but since PG&E was already performing eddy current examinations

on 100 percent of the available tubes, it had no impact on sample size. The inspectors

determined that the flaw degradation severity levels found, thus far, were well within the

predicted expectations.

The inspection procedure specified confirmation that the steam generator tube eddy

current test scope and expansion criteria meet TS requirements, EPRI guidelines, and

commitments made to the NRC. The inspectors evaluated the recommended steam

generator tube eddy current test scope established by TS requirements and the Diablo

Canyon Power Plant Power Plant degradation assessment report. The inspectors

compared the recommended test scope to the actual test scope and found that PG&E

had accounted for all known flaws and had, as a minimum, established a test scope that

met TS requirements, EPRI guidelines, and commitments made to the NRC.

The inspection procedure specified, if new degradation mechanisms were identified,

verification that the licensee fully enveloped the problem in its analysis of extended

conditions including operating concerns and had taken appropriate corrective actions

before plant startup. To date, the eddy current test results had not identified any new

degradation mechanisms.

The inspection procedure requires confirmation that the licensee inspected all areas of

potential degradation, especially areas that were known to represent potential eddy

current test challenges (e.g., top-of-tubesheet, tube support plates, and U-bends). The

inspectors confirmed that all known areas of potential degradation were included in the

scope of inspection and were being inspected.

The inspection procedure further requires verification that repair processes being used

were approved in the TS. At the time of this inspection, it was estimated that a total of

approximately 108 tubes would be plugged using mechanically rolled plugs, none of

which had been installed. The inspectors verified that this particular plugging operation

was an NRC-approved repair process.

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The inspection procedure also requires confirmation of adherence to the TS plugging

limit, unless alternate repair criteria have been approved. The inspection procedure

further requires determination whether depth-sizing repair criteria were being applied for

indications other than wear or axial primary water stress corrosion cracking in dented

tube support plate intersections. The inspectors determined that the TS plugging limits

were being adhered to (i.e., 40 percent maximum through-wall indication).

If steam generator leakage greater than 3 gallons per day was identified during

operations or during post shutdown visual inspections of the tubesheet face, the

inspection procedure requires verification that the licensee had identified a reasonable

cause based on inspection results and that corrective actions were taken or planned to

address the cause for the leakage. The inspectors did not conduct an assessment

because this condition did not exist.

The inspection procedure requires confirmation that the eddy current test probes and

equipment were qualified for the expected types of tube degradation and an assessment

of the site-specific qualification of one or more techniques. The inspectors observed

portions of eddy current tests performed on the tubes in Steam Generators 1-1, 1-2, 1-3,

and 1-4. During these examinations, the inspectors verified that: (1) the probes

appropriate for identifying the expected types of indications were being used, (2) probe

position location verification was performed, (3) calibration requirements were adhered,

and (4) probe travel speed was in accordance with procedural requirements. The

inspectors performed a review of site-specific qualifications of the techniques being

used. These are identified in the Attachment.

If loose parts or foreign material on the secondary side were identified, the inspection

procedure specified confirmation that the licensee had taken or planned appropriate

repairs of affected steam generator tubes and that they inspected the secondary side to

either remove the accessible foreign objects or perform an evaluation of the potential

effects of inaccessible object migration and tube fretting damage. During this

inspection, three small pieces of wire (possibly from a wire brush) were identified in

Steam Generator 1-2 during foreign object search and retrieval (FOSAR) inspections.

These were removed.

Finally, the inspection procedure specified review of one to five samples of eddy current

test data if questions arose regarding the adequacy of eddy current test data analyses.

The inspectors did not identify any results where eddy current test data analyses

adequacy was questionable.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

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1R11 Licensed Operator Requalification (71111.11)

a. Inspection Scope

The inspectors observed testing and training of senior reactor operators and reactor

operators to identify deficiencies and discrepancies in the training, to assess operator

performance, and to assess the evaluators critique. The training scenario involved

reactor coolant system leakage, an earthquake, a loss-of-coolant accident, and a

radiological release from the containment.

Documents reviewed by the inspectors included Lesson ES 1213A, LOCA,

Revision 12.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors reviewed the five below listed maintenance activities to: (1) verify the

appropriate handling of structure, system, and component (SSC) performance or

condition problems; (2) verify the appropriate handling of degraded SSC functional

performance; (3) evaluate the role of work practices and common cause problems; and

(4) evaluate the handling of SSC issues reviewed under the requirements of the

Maintenance Rule, 10 CFR Part 50, Appendix B, and the TS.

  • October 5, 2005: Units 1 and 2, fan belts,
  • December 12, 2005: Unit 1, Startup Transformer 1-1 Load Tap Changer,
  • December 16, 2005: Unit 1, Seismic Monitor ENSTA3 and Trip Device Y-203,
  • December 16, 2005: Units 1 and 2, Auxiliary Transformer 1-1 oil analysis,

Documents reviewed by the inspectors are listed in the Attachment.

The inspectors completed four samples.

b. Findings

No findings of significance were identified.

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1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

.1 Risk Assessments and Management of Risk

a. Inspection Scope

The inspectors reviewed the below listed assessment activities to verify:

(1) performance of risk assessments when required by 10 CFR 50.65(a)(4) and PG&E

procedures prior to changes in plant configuration for maintenance activities and plant

operations; (2) the accuracy, adequacy, and completeness of the information

considered in the risk assessment; (3) that PG&E recognizes, and/or enters as

applicable, the appropriate risk category according to the risk assessment results and

PG&E procedures; and (4) PG&E identified and corrected problems related to

maintenance risk assessments.

  • October 6, 2005: Unit 1, Component Cooling Water Pump 1-1 maintenance and

500 kV Breaker 532 replacement

Documents reviewed by the inspectors included Procedure AD7.DC6, On-line

Maintenance Risk Management, Revision 9.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

.2 Emergent Work

f. Inspection Scope

The inspectors: (1) verified that PG&E performed actions to minimize the probability of

initiating events and maintained the functional capability of mitigating systems and

barrier integrity systems; (2) verified that emergent work-related activities such as

troubleshooting, work planning/scheduling, establishing plant conditions, aligning

equipment, tagging, temporary modifications, and equipment restoration did not place

the plant in an unacceptable configuration; and (3) reviewed the FSAR Update to

determine if PG&E identified and corrected risk assessment and emergent work control

problems.

  • October 24, 2005: Unit 1, Vital Inverter IY-13 trip
  • November 6, 2005: Unit 2, spent fuel pool level drop
  • November 23, 2005: Unit 2, Diesel Engine Generator 2-3 lube oil heater

contactor failure and pre-circulating lube oil pump vibration

Documents reviewed by the inspectors are listed in the Attachment.

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The inspectors completed three samples.

b. Findings

Section 4OA7 discusses findings of very low safety significance identified by PG&E.

1R14 Personnel Performance Related to Nonroutine Plant Evolutions and Events (71111.14)

a. Inspection Scope

The inspectors: (1) reviewed operator logs, plant computer data, and/or strip charts for

the below listed evolutions to evaluate operator performance in coping with non-routine

events and transients; (2) verified that operator actions were in accordance with the

response required by plant procedures and training; and (3) verified that PG&E has

identified and implemented appropriate corrective actions associated with personnel

performance problems that occurred during the non-routine evolutions sampled.

  • October 12, 2005: Unit 1, Operators and engineers observed several nuclear

instrument spikes near the end of core life, as well as a half-step inward on the

controlling group control rods.

  • November 19, 2005: Unit 2, While performing maintenance on Startup

Transformer 1-1, Sudden Pressure Relay 80MRST11 was actuated and resulted

in the opening of Breaker 212 in the 230 kV switchyard and the loss of startup

power to Unit 2.

  • November 27, 2005: While performing a refill of Safety Injection

Accumulator 1-1 using the safety injection system pumps, the operators

inadvertently injected into the reactor coolant system.

Documents reviewed by the inspectors are listed in the Attachment.

The inspectors completed three samples.

b. Findings

(1) Loss of Startup Power to Unit 2

Introduction: A Green, self-revealing NCV was identified for the failure to

adequately assess and manage the risk associated with maintenance on Startup

Transformer 1-1, as required by 10 CFR 50.65(a)(4). Specifically, PG&E failed

to conduct a circuit isolation plan, which was a risk management action required

by procedures. As a result, startup power to Unit 2 was lost.

Description: On November 19, 2005, maintenance technicians were performing

a functional test of Relay 80MRST11 when a sudden pressure relay trip alarmed

on Startup Transformer 1-1 and Breaker 212, which provides startup power to

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both units, tripped open in the 230 kV switchyard. This resulted in a loss of

startup power to Unit 2. Unit 1 was not affected because startup power was

cleared for that unit. The Unit 2 diesel engine generators auto-started on the

loss of startup power but did not load because the associate vital buses

remained energized. The Unit 2 diesel generator engines were subsequently

shutdown by the operators. PG&E staff determined that Sudden Pressure

Relay 80MRST11 was not adequately isolated from the protective circuit for

Startup Transformer 1-1. Therefore, when the maintenance technician tested

the relay, a signal was sent to Breaker 212 to open.

The apparent cause was identified as a human performance error in failing to

review applicable drawings and take appropriate actions prior to relay actuation.

Additionally, the inspectors recognized that Procedure AD7.DC8, Work Control,

Revision 20, stated that any work with a performance frequency of greater than

quarterly shall be considered as non-routine and should be evaluated against

Procedure MA1.DC11, Risk Assessment, Revision 5A. Procedure MA1.DC11

required that a circuit isolation plan be developed for work that imposed medium-

to high -risk. The use of the circuit isolation plan would have added an

opportunity to identify the potential impact to Unit 2 startup power.

Analysis: The performance deficiency associated with this finding involved the

failure to adequately assess and manage the risk associated with maintenance

on the Startup Transformer 1-1 relay. The finding was greater than minor

because it is related to IMC 0612, Appendix B, Section 3(5)(I), for a failure to

implement any prescribed significance compensatory measures or failure to

effectively manage those issues. In this case, maintenance personnel failed to

fully implement Procedures AD7.DC8 and MA1.DC11, which called for a circuit

isolation plan for medium- to high-risk maintenance activities as a risk

management action. The finding affected the Mitigating Systems Cornerstone.

Using IMC 0609, Appendix K, Maintenance Risk Assessment and Risk

Management Significance Determination Process, Flowchart 2 - Assessment of

Risk Management Actions," the incremental core damage probability was less

than 1E-6 and the incremental large early release frequency was less than 1E-7.

The finding was assessed as having very low safety significance. The cause of

the finding is related to the crosscutting element of human performance in that

maintenance personnel failed to follow procedures.

Enforcement: 10 CFR 50.65(a)(4) requires, in part, that before performing

maintenance activities, the licensee shall assess and manage the risk that may

result from the proposed maintenance activities. Contrary to this, on

November 19, 2005, maintenance personnel failed to adequately assess and

manage the risk associated with protective relay maintenance on Startup

Transformer 1-1, which resulted in the loss of startup power to Unit 2.

Specifically, maintenance personnel failed to implement a risk management

action (circuit isolation plan), which would have provided an opportunity to

identify the potential loss of startup power to Unit 2. The corrective actions to

restore compliance included revision of the protective relay work orders requiring

circuit isolation plans, a review of work involving startup transformers, and

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additional training on protective relay work. Because the finding is of very low

safety significance and has been entered into the CAP as AR A0652421, this

violation is being treated as an NCV consistent with Section VI.A of the

Enforcement Policy: NCV 50-275/05-05-01, Failure to Adequately Assess and

Manage Risk Associated With Startup Transformer 1-1 Maintenance.

Introduction: A Green, self-revealing NCV of Technical Specifications 5.4.1.a

was identified for improper implementation of Operating Procedure OP B-3B:I,

Accumulators- Fill and Pressurize, Revision 23. The failure to follow

Procedure OP B-3B:I resulted in exceeding the cooldown rate for the pressurizer

and contributing to safety injection discharger header pressurization due to

perturbation of check Valve SI-1-8948B.

Description: On November 27, 2005, operators were using Procedure OP B-3B:I

to align the safety injection system for filling Accumulator 1-3 using the safety

injection pumps. Procedure OP B-3B:I, step 6.1, directs the operators to

perform step 6.7 if primary plant pressure is at or near normal operating

pressure. Contrary to this, at the time of the evolution primary plant pressure was

lower than normal operating pressure. Operators aligned the safety injection

system according to Step 6.7, and the resultant alignment caused water to be

transferred into the reactor coolant system rather than Accumulator 1-3. The

increase in primary plant inventory raised pressurizer level from 40 to 72 percent,

or approximately 1800 gallons. The high pressurizer level alarm was received at

the 70 percent level setpoint. As a result of the change in level, the pressurizer

liquid space temperature decreased from 539EF to 370EF in 15 minutes. The

operators then energized all of the pressurizer heaters and restored the

pressurizer liquid temperature to the normal steady state temperature of 530EF

over the next hour. Equipment Control Guideline 7.5 specified a pressurizer

heat-up limit of 100EF in one hour. This heat-up was exceeded in approximately

15 minutes when liquid temperatures reached 471EF.

Additionally, as a result of the safety injection system misalignment, the first off

and second off emergency core cooling system check valves had become

unseated. Valve SI-1-8948B was later identified to be leaking. This leakage

from the primary to the safety injection system had two primary effects;

Accumulators 1-1 and 1-3 boron concentration was being diluted and the safety

injection header pressure was slowly being pressurized. These conditions

required additional procedures to be changed and implemented to assure that

boron concentration remained within TS limits, and the safety injection header

pressure did not pressurize to a point where the header relief valves would

actuate at 1750 psig. These conditions are identified in PG&Es CAP by

ARs A0653564, A0610421, and A0653644. Further discussion of historical

check valve performance is discussed in this report under Section 4OA2,

Identification and Resolution of Problems.

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Analysis: The performance deficiency associated with this finding involved

operations personnel failing to perform the appropriate sections of

Procedure OP B-3B:I with regard to existing plant conditions. The finding is

greater than minor because it was associated with the Mitigating System

Cornerstone attribute of configuration control and affects the associated

cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

Using IMC 0609, "Significance Determination Process," Appendix G, Checklist 4,

the finding did not require quantitative screening. Therefore, the finding was

assessed as having very low safety significance. The cause of the finding is

related to the crosscutting element of human performance in that operations

personnel did not follow procedures.

Enforcement: TS 5.4.1.a requires that written procedures be established,

implemented, and maintained covering the activities specified in Appendix A,

Typical Procedures for Pressurized Water Reactors and Boiling Water

Reactors, of Regulatory Guide 1.33, Quality Assurance Program Requirements

(Operation), dated February 1978. Regulatory Guide 1.33, Appendix A,

Section 3.d requires procedures for emergency core cooling systems.

Procedure OP B-3B:I, Accumulators- Fill and Pressurize, Revision 23, required

that operators go to Step 6.7 only if filling accumulators from about normal

pressure and level. Contrary to this, on November 27, 2005, operators failed to

implement the steps prior to Step 6.7 to properly align the safety injection system

when reactor coolant system pressure and level were not at normal values.

Improper alignment of the safety injection system allowed injection into the

reactor coolant system; exceeding the pressurizer heatup limits and contributing

to Valve 8948B back-leakage. PG&E has initiated actions to determined the

apparent cause and appropriate corrective actions. Because this finding is of

very low safety significance and it was entered into PG&Es CAP, it is being

treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement

Policy: NCV 50-275/05-05-02, Failure to Properly Implement Procedure for

Safety Injection System Operation.

1R15 Operability Evaluations (71111.15)

m. Inspection Scope

The inspectors: (1) reviewed plant status documents such as operator shift logs,

emergent work documentation, deferred modifications, and standing orders to

determine if an operability evaluation was warranted for degraded components;

(2) referred to the FSAR Update and design bases documents to review the technical

adequacy of the operability evaluations; (3) evaluated compensatory measures

associated with operability evaluations; (4) determined degraded component impact on

any TS; (5) used the SDP to evaluate the risk significance of degraded or inoperable

equipment; and (5) verified that PG&E has identified and implemented appropriate

corrective actions associated with degraded components.

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  • October 5, 2005: Units 1 and 2, Fire protection and the potential loss of reactor

coolant pump seal cooling

conservatism Leakage Detection Sensitivity"

oil leak

  • November 1, 2005: Unit 2, Particulate matter found in Centrifugal Charging

Pump 2-2 lube oil system

  • November 4, 2005: Unit 1, Structural beam damage at Main Steam Lead 4 pipe

restraint

  • November 8, 2005: Unit 1, Source Range Detector N31 intermittent alarm for

loss of detector voltage

December 15, 2005: Unit 1 and 2, TS Limiting Condition of Operation 3.4.1

TAVG limit inconsistent with current analysis

  • December 15, 2005: Unit 1 and 2, Doppler acoustic sounder not functioning

b. Findings

Introduction: An unresolved item was identified to further evaluate the corrective actions

that were implemented following failures of auxiliary feedwater valve level control valves.

Description: Valve FW-1-LCV-107 is a discharge valve from the turbine-driven auxiliary

feedwater pump to Steam Generator 1-2. Its safety function is to close in order to

isolate auxiliary feedwater flow to that steam generator if it is faulted.

On November 3, 2005, operators were stroking Valve FW-1-LCV-107 per

Procedure STP V-2U2D, Exercising S/G No. 2 AFW Supply Valves LVC-107 and

LCV-111, Revision 4, after valve packing had been replaced. Valve FW-1-LCV-107

had been stroked open and closed successfully from the control room. Operational

control for the valve was then transferred to the hot shutdown panel, and the valve was

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opened, but not able to be shut. Several other attempts to shut the valve from the hot

shutdown panel and the control room were also unsuccessful. PG&E staff later

determined that the Limitorque valve actuators torque limit switch exhibited high

resistance across its contacts. This Limitorque actuator (Model SMB-000) used leaf-

spring contacts in a non-wiping configuration for the torque switch. A visual inspection

of the contacts revealed some particulates and dust laying about the contact fingers.

Maintenance records indicated that the contacts were burnished prior to valve packing

maintenance, providing an opportunity for maintenance to introduce the loose material

into the valve actuator.

Inspectors observed that the same torque limit switch had prevented

Valve FW-1-LCV-107 from operating 14 months previously. This failure, as described in

AR A0616766, also occurred after preventive maintenance to clean and lubricate the

valve actuator on August 19, 2004. The apparent cause in AR A0616766 stated the

DCPP [Diablo Canyon Power Plant] PM [preventive maintenance] program inadequately

inspects and cleans torque switch contacts. The close torque switch contacts for

Valve 1-LCV-107 were dirty and/or oxidized. PG&E staff had performed a search of

industry operating experience in AR A0616766 and found several events where dirty

torque switch contacts prevented a Limitorque actuator from functioning. The

recommended corrective action in AR A0616766 was to revise Procedure MP E-53.10A,

Preventive Maintenance of Limitorque Motor Operators, Revision 28, to require

inspecting the torque switch contact surfaces and cleaning contacts, if needed, during

the inspection and lubrication of the actuator. The response to the recommended

corrective actions in AR A0616766 stated that the procedure already contained a step to

inspect the condition and alignment of torque switch contacts. Subsequently, a step to

burnish the contacts of the torque switches was added to Procedure MP E-53.10A.

The inspectors observed an additional case where dirty contacts on a torque limit switch

may have prevented Valve FW-2-LCV-109 from closing on March 15, 2003.

Valve FW-2-LCV-109 is also a discharge valve for the turbine-driven auxiliary feedwater

pump on Unit 2. AR A0578562 stated that operators attempted to close

Valve FW-2-LCV-109 during a test of the turbine-driven AFW pump, but the valve failed

to close. However, the valve was opened before adequate troubleshooting could be

initiated to determine the cause. Therefore, PG&E could not determine the cause of the

actuator failure since the valve actuator performed appropriately thereafter. An

additional failure of Valve FW-1-LCV-108 occurred in February 2006.

Analysis: No analysis has been performed based on additional inspection is needed to

determine whether a performance deficiency exists. The inspection will consider any

common cause aspects between the three valves that have experienced failures.

Enforcement: No enforcement action has been identified. URI 50-275/05-05-03,

Corrective Actions to Prevent Repetitive Failures of Auxiliary Feedwater Limitorque

Valves (Section 1R15).

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1R19 Postmaintenance Testing (71111.19)

a. Inspection Scope

The inspectors selected the six below listed postmaintenance test activities of risk-

significant systems or components. For each item, the inspectors: (1) reviewed the

applicable licensing basis and/or design basis documents to determine the safety

functions; (2) evaluate the safety functions that may have been affected by the

maintenance activity; and (3) reviewed the test procedure to ensure it adequately tested

the safety function that may have been affected. The inspectors either witnessed or

reviewed test data to verify that acceptance criteria were met, plant impacts were

evaluated, test equipment was calibrated, procedures were followed, jumpers were

properly controlled, the test data results were complete and accurate, the test

equipment was removed, the system was properly re-aligned, and deficiencies during

testing were documented. The inspectors also reviewed the FSAR Update to determine

if PG&E identified and corrected problems related to postmaintenance testing.

  • October 11, 2005: Unit 2, Tension hold-down bolts for Centrifugal Charging

Pump 2-1

  • November 7, 2005: Unit 1, Battery 1-3 modified performance test
  • November 23, 2005: Unit 2, Diesel Engine Generator 2-3 lube oil heater

contactor failure

  • November 27, 2005: Unit 1, Repair of torn structural I-beam
  • November 23, 2005: Unit 1, Diesel Engine Generator 1-2 breaker was slow to

close

  • November 24, 2005: Unit 1, Component Cooling Water Pump 1-2 failed to start

on a safety injection signal

  • December 19, 2005: Unit 1, Vital Battery Cells 37 and 60 replacement

Documents reviewed by the inspectors are listed in the Attachment.

The inspectors completed seven samples

b. Findings

(1) Vital Battery Cells 37 and 60 Replacement

10 CFR Part 50, Appendix B, Criterion II, Quality Assurance Program, requires,

in part, that the quality assurance program shall provide for indoctrination and

training of personnel performing activities affecting quality as necessary to

assure that suitable proficiency is achieved and maintained. Contrary to this, on

November 16, 2005, PG&E failed to provide for adequate indoctrination and

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training of personnel for Vital Battery 1-2 cell replacement in order to assure that

suitable proficiency is achieved and maintained. Specifically, step 5.12.4 of

Procedure TQ2.ID4, Training Program Implementation, Revision 8, required

maintenance personnel to document the circumstances for requiring the use of

an unqualified worker given that a subject matter expert was providing work

oversight. The vital battery system engineer provided oversight of unqualified

workers to replace Cells 37 and 60 on Vital Battery 1-2 since qualified staff were

unavailable to perform the work. However, maintenance personnel failed to

document the circumstances for requiring the use of the unqualified workers to

perform the work and the system engineer (subject matter expert) to oversee the

work. Using IMC 0612, Appendix B, this issue was determined to be a minor

violation of NRC requirements because the failure to provide documentation did

not affect the capability of Vital Battery 1-2 to perform its safety function.

Furthermore, critical aspects of the cell replacement were adequately performed.

The finding has been entered into PG&Es CAP as AR A0655870.

(2) Agastat ETR Time-Delay Relay Failures

Introduction: An unresolved item was identified regarding Agastat ETR time-

delay relays and how they caused the slow feeder breaker closure for DEG 1-2

and the failure of CCW 1-2 to start on a safety injection signal. Resolution is

pending upon completion of the relay failure analysis performed by PG&E and

the vendor.

Description. While performing surveillance test STP M-13G, 4kV Bus G Non-SI

Auto-Transfer Test, Revision 28A, on November 21, 2005, PG&E staff noted

that DEG 1-2 feeder breaker closed at 23 seconds versus the 17-second

acceptance criteria in the test procedure. Engineers and maintenance

technicians subsequently performed troubleshooting and determined that

Relay 62HG3B was the source of the slow breaker closure. Relay 62HG3B was

an Agastat ETR14D time-delay relay. Maintenance technicians bench-tested the

relay and found that it exhibited considerable drift from its time-delay setpoint of

17 seconds (as-found was 19.98 seconds). Maintenance technicians replaced

the relay, and operators successfully reperformed STP M-13G.

On November 23, 2005, while performing surveillance test STP M-15,

Integrated Test of Engineered Safeguards and Diesel Generators,

Revision 38A, CCW Pump 1-2 failed to start on a safety injection signal.

Engineers and maintenance technicians performed troubleshooting and found

that Relay 2HG12/TD (Agastat ETR14D time-delay relay) failed to actuate.

Technicians subsequently replaced the relay, and operators were able to

successfully run CCW Pump 1-2 from a safety injection signal.

PG&E staff reviewed industry operating experience on the Agastat ETR14D

time-delay relays and found approximately 25 issues in the past 21 years. Most

of the issues involved poor solder connections. The inspectors also reviewed

operating experience on the Agastat ETR14D time-delay relays but did not find

any applicable experience. Most operating experience associated with Agastat

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time-delay relays has been associated with the electro-pneumatic models. A

subsequent search of operating experience with the relays at Diablo Canyon

Power Plant showed only four reliability issues, with only one issue in the past

year. Currently, PG&E does not consider the two relay failures to be indicative of

a larger problem with the Agastat ETR14D time-delay relays based on good

performance from the relays in the past and successful testing of the other

relays on Unit 1 during Refueling Outage 1R13.

PG&E planned to send the two failed relays to the vendor for failure analysis.

The inspectors will review the failure analysis upon its completion.

Analysis: The safety significance of any performance issues identified upon

review of PG&Es failure analysis will be determined at that time.

Enforcement: This issue remains unresolved pending NRC review of the relay

failure analysis: URI 50-275/05-05-04; Assess Failure of Agastat ETR Time-

Delay Relays.

1R20 Refueling and Outage Activities (71111.20)

a. Inspection Scope

The inspectors reviewed the following risk-significant refueling items or outage activities

to verify defense-in-depth commensurate with the outage risk control plan, compliance

with the TS, and adherence to commitments in response to Generic Letter 88-17, Loss

of Decay Heat Removal: (1) the risk control plan; (2) tagging/clearance activities;

(3) reactor coolant system instrumentation; (4) electrical power; (5) decay heat removal;

(6) spent fuel pool cooling; (7) inventory control; (8) reactivity control; (9) containment

closure; (10) reduced inventory or midloop conditions; (11) refueling activities;

(12) heatup and cooldown activities; (13) restart activities; and (14) identification and

implementation of appropriate corrective actions associated with refueling and outage

activities. The inspectors containment inspections included observations of the

containment sump for damage and loose material; and supports, braces, and snubbers

for evidence of excessive stress, water hammer, or aging. Documents reviewed by the

inspectors included the Unit 1 Refueling Outage 1R13 Outage Safety Plan.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the FSAR Update, procedure requirements, and TS to ensure

that the three below listed surveillance activities demonstrated that the SSCs tested

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were capable of performing their intended safety functions. The inspectors either

witnessed or reviewed test data to verify that the following significant surveillance test

attributes were adequate: (1) preconditioning; (2) evaluation of testing impact on the

plant; (3) acceptance criteria; (4) test equipment; (5) procedures; (6) jumpers; (7) test

data; (8) testing frequency and method demonstrated TS operability; (9) test equipment

removal; (10) restoration of plant systems; (11) fulfillment of ASME Code requirements;

(12) updating of performance indicator data; (13) engineering evaluations, root causes,

and bases for returning tested SSCs not meeting the test acceptance criteria were

correct; (14) reference setting data; and (15) annunciators and alarm setpoints. The

inspectors also verified that PG&E identified and implemented any needed corrective

actions associated with the surveillance testing.

  • October 7, 2005: Unit 1 - Inservice Test, Procedure STP V-3F1, Exercising

Valve FCV-495, ASW Pump 2 Crosstie Valve, Revision 21

  • November 21, 2005: Unit 1, Procedure STP M-13G, 4kV Bus G Non-SI Auto-

Transfer Test, Revision 28A

  • November 22, 2005: Unit 2, Procedure STP M-15, Integrated Test of

Engineered Safeguards and Diesel Generators, Revision 38A

The inspectors completed three samples.

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP2 Alert Notification System Testing (71114.02)

a. Inspection Scope

The inspector discussed with PG&E staff the status of offsite siren and tone alert radio

systems and PG&E changes to the siren testing methodology to determine the

adequacy of PG&E methods for testing the alert and notification system in accordance

with 10 CFR Part 50, Appendix E. PG&Es alert and notification system testing program

was compared with criteria in NUREG-0654, Criteria for Preparation and Evaluation of

Radiological Emergency Response Plans and Preparedness in Support of Nuclear

Power Plants, Revision 1; Federal Emergency Management Agency (FEMA) Report

REP-10, Guide for the Evaluation of Alert and Notification Systems for Nuclear Power

Plants; and PG&Es current FEMA-approved alert and notification system design report.

The inspector completed one sample.

b. Findings

No findings of significance were identified.

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1EP3 Emergency Response Organization Augmentation Testing (71114.03)

a. Inspection Scope

The inspector reviewed the following documents related to the emergency response

organization augmentation system to determine PG&Es ability to staff emergency

response facilities in accordance with PG&Es emergency plan and the requirements of

10 CFR Part 50, Appendix E:

  • OM10.DC2, ERO on-call, Revision 4
  • OM10.ID4, ERO Management, Revision 7
  • Evaluations for call-in and drive-in drills conducted in 2005

The inspector completed one sample.

b. Findings

No findings of significance were identified.

1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies (71114.05)

a. Inspection Scope

The inspector reviewed the following documents related to PG&Es corrective action

program to determine PG&Es ability to identify and correct problems in accordance with

10 CFR 50.47(b)(14) and 10 CFR 50, Appendix E:

  • EPG 01, Problem Identification, May 17, 2002

department during calendar years 2004 and 2005

  • Procedure OM7.ID1, Problem Identification and Resolution - Action Requests,

Revision 20A

  • Details of 42 selected actions requests
  • Five quality assurance audits and assessments
  • Three drill and exercise drill reports

The inspector completed one sample.

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b. Findings

No findings of significance were identified.

1EP6 Emergency Preparedness Evaluation (71114.06)

a. Inspection Scope

For the one below simulator-based training evolution contributing to Drill/Exercise

Performance and Emergency Response Organization Performance Indicators, the

inspectors: (1) observed the training evolution to identify any weaknesses and

deficiencies in classification, notification, and Protective Action Recommendation

development activities; (2) compared the identified weaknesses and deficiencies against

PG&E identified findings to determine whether PG&E is properly identifying failures; and

(3) determined whether PG&E performance is in accordance with the guidance of the

NEI 99-02, Voluntary Submission of Performance Indicator Data, acceptance criteria.

  • November 10, 2005: Unit 1, Shift Manager classification and declaration of

separate events involving main turbine damage, high effluent discharge,

anticipated transient without scram, steam generator tube rupture, fuel assembly

damage, and a tsunami

Documents reviewed by the inspectors included:

  • Procedure EP G-3, Emergency Notification of Off-Site Agencies, Revision 44

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

2. RADIATION SAFETY

Cornerstone: Occupational Radiation Safety [OS]

2OS1 Access Control To Radiologically Significant Areas (71121.01)

a. Inspection Scope

This area was inspected to assess PG&Es performance in implementing physical and

administrative controls for airborne radioactivity areas, radiation areas, high radiation

areas, and worker adherence to these controls. The inspector used the requirements in

10 CFR Part 20, the TSs, and PG&Es procedures required by TSs as criteria for

determining compliance. During the inspection, the inspector interviewed the radiation

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protection manager, radiation protection supervisors, and radiation workers. The

inspector performed independent radiation dose rate measurements and reviewed the

following items:

  • Performance indicator events and associated documentation packages reported

by PG&E in the Occupational Radiation Safety cornerstone

  • Controls (surveys, posting, and barricades) of three radiation, high radiation, or

airborne radioactivity areas

  • Radiation work permits, procedures, engineering controls, and air sampler

locations

  • Conformity of electronic personal dosimeter alarm set points with survey

indications and plant policy; workers knowledge of required actions when their

electronic personnel dosimeter noticeably malfunctions or alarms

  • Adequacy of PG&Es internal dose assessment for any actual internal exposure

greater than 50 millirem committed effective dose equivalent

  • Physical and programmatic controls for highly activated or contaminated

materials (non-fuel) stored within spent fuel and other storage pools

  • Self-assessments, audits, licensee event reports, and special reports related to

the access control program since the last inspection

  • Corrective action documents related to access controls
  • PG&E actions in cases of repetitive deficiencies or significant individual

deficiencies

  • Radiation work permit briefings and worker instructions
  • Adequacy of radiological controls such as, required surveys, radiation protection

job coverage, and contamination controls during job performance

  • Dosimetry placement in high radiation work areas with significant dose rate

gradients

and very high radiation areas

  • Controls for special areas that have the potential to become very high radiation

areas during certain plant operations

  • Posting and locking of entrances to all accessible high dose rate - high radiation

areas and very high radiation areas

  • Radiation worker and radiation protection technician performance with respect to

radiation protection work requirements

-31- Enclosure

Either because the conditions did not exist or an event had not occurred, no

opportunities were available to review the following items:

areas

The inspector completed 21 of the required 21 samples.

b. Findings

Introduction: The inspector identified a NCV of 10 CFR 20.1902 because PG&E failed

to post a radiation area. The violation had very low safety significance.

Description: On November 15, 2005, the inspector toured the 115-foot yard area.

Inside Vault 26, the inspector identified, through independent measurements, an area in

which the radiation dose rates were approximately 30 millirem per hour at

30 centimeters from the surfaces of radioactive material containers. The dose rate was

confirmed by a radiation protection technician using an ion chamber radiation detection

device. The inspector observed that neither the discrete area nor the open entrance to

Vault 26 was posted with a radiation area warning sign, although the auxiliary building

doorway to the yard was posted as a radiation area.

The inspector reviewed the applicable guidance in NUREG/CR-5569, Revision 1, Health

Physics Positions 036, Posting of Entrances to a Large Room or Building as a

Radiation Area, and 066, Guidance for Posting Radiation Areas. Because the yard

area was large and very little of it was a radiation area, the inspector concluded that

posting on the doorway to the yard rather than the discrete areas was not sufficient to

inform radiation workers of radiological hazards in their work areas.

Analysis: The failure to post a radiation area is a performance deficiency. The finding

was more than minor because it was associated with one of the cornerstone attributes

(exposure control and monitoring) and the finding affected the Occupational Radiation

Safety cornerstone objective, in that, uninformed workers could unknowingly accrue

additional radiation dose. Because the finding involved the potential for unplanned,

unintended dose resulting from conditions that were contrary to NRC regulations, the

finding was evaluated using the Occupational Radiation Safety Significance

Determination Process. The inspector determined that the finding had no more than

very low safety significance because: (1) it did not involve American Society of

Mechanical Engineers (ALARA) planning and controls, (2) there was no personnel

overexposure, (3) there was no substantial potential for personnel overexposure, and

(4) the finding did not compromise PG&Es ability to assess dose. The finding also has

cross-cutting aspects related to problem identification and resolution, in that, a similar

violation was previously identified during Inspection 05000275/2002004;

0500323/2002004.

Enforcement: 10 CFR 20. 003 defines a radiation area as an area, accessible to

individuals, in which radiation levels could result in an individual receiving a dose

equivalent in excess of 5 millirem in an hour at 30 centimeters from the radiation source

or from any surface that the radiation penetrates. 10 CFR 20. 902 requires each

radiation area be posted with a conspicuous sign or signs. PG&E violated this

requirement when it did not post the discrete area or the open entrance to Vault 26.

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This violation is in PG&Es CAP as AR A0652226. Because this finding is of very low

safety significance and it was entered into PG&Es corrective action program, it is being

treated as a non-cited violation, consistent with Section VI.A.1 of the NRC Enforcement

Policy: NCV 05000275; 323/2005-05-05, Failure to Post a Radiation Area.

4. OTHER ACTIVITIES

4OA1 Performance Indicator(PI) Verification (71151)

.1 Emergency Preparedness Cornerstone

a. Inspection Scope

The inspector sampled PG&E submittals for the PIs listed below for the period of

October 1, 2004, through September 30, 2005. The definitions and guidance of Nuclear

Engineering Institute 99-02, Regulatory Assessment Indicator Guideline, Revisions 2

and 3, were used to verify PG&Es basis for reporting each data element in order to

verify the accuracy of PI data reported during the assessment period. PG&E PI data

were also reviewed against the requirements of Procedure AWP EP-001, Emergency

Preparedness Performance Indicators, Revision 5.

  • Drill and Exercise Performance
  • Emergency Response Organization Participation
  • Alert and Notification System Reliability

The inspector reviewed a 100 percent sample of drill and exercise scenarios and

licensed operator simulator training sessions, notification forms, and attendance and

critique records associated with training sessions, drills, and exercises conducted during

the verification period. The inspector reviewed selected emergency responder

qualification, training, and drill participation records. The inspector reviewed the

evaluation of the June 14, 2005, Tsunami event. The inspector reviewed alert and

notification system testing procedures and a 100 percent sample of siren test records.

The inspector also interviewed PG&E personnel responsible for collecting and

evaluating PI data.

The inspector completed three samples.

b. Findings

Introduction: A Severity Level IV NCV of 10 CFR 50.9 was identified because PG&E

failed to provide complete and accurate PI information to the NRC. Specifically, the

inspector identified two errors in the second quarter 2005 drill and exercise performance

PI opportunities evaluated by PG&E and, when the PI was recalculated, the drill and

exercise performance PI crossed the Green-to-White performance band threshold for

the second quarter of 2005.

Description: During review of the second quarter 2005 drill and exercise performance PI

documentation, the inspector identified two emergency notification forms that were

incorrectly annotated as emergency vice drill. Neither of these errors had been

evaluated as a missed opportunity for the drill and exercise performance PI, and both

had been reported as successful opportunities. Both of these drill and exercise

-33- Enclosure

performance opportunities were from the 2005 annual licensed operator requalification

operating tests in the plant control room simulator. When the drill and exercise

performance PI data for second quarter 2005 was re-evaluated with these two

corrections, the indicator crossed the Green-to-White threshold. PG&E subsequently

identified a third example of the same error.

The operating tests had been identified for evaluation of emergency preparedness PIs,

and operations department learning services training personnel conducted the

evaluations. Documentation of the evaluations was then provided to the Emergency

Preparedness Department staff, who then reviewed the evaluations and summarized the

quarterly results for reporting of the PIs. For the entire second quarter, 33 drill and

exercise performance opportunities were identified, and 25 were originally evaluated

and reported as successful. Following the inspectors identification of two inaccurate

notification forms, PG&E performed a review and identified an additional inaccurate

notification form with the same error as identified by the inspector. As an immediate

corrective action to the errors noted in the second quarter evaluations, PG&E also

conducted a review of the third quarter PI data, which had been prepared for

submission, to verify the accuracy of the evaluation of the 162 opportunities that had

been performed in the third quarter. One additional error was identified on a notification

form where an error had been identified and corrected with the time of the declaration;

however, the method of correction did not meet accuracy standards of the facility and;

therefore, the notification opportunity was reevaluated as a missed opportunity.

Historically, the drill and exercise performance PI at Diablo Canyon Power Plant was

approximately 95 percent. After the second quarter 2005 performance was added to the

PI, the indicator dropped to 90.8 percent (before correction). PG&E took corrective

action in the third quarter by conducting refresher training and job performance measure

evaluations with all shift manager qualified senior licensed operators. This resulted in

162 PI opportunities for the third quarter.

The inspector reviewed the performance deficiencies associated with the missed drill

and exercise performance PI opportunities. During the second quarter evaluations, two

classification opportunities were missed because of late classifications of a site area

emergency, and the remaining nine missed opportunities were accuracy errors on the

emergency notification form. During the third quarter evaluations, six missed

classifications were identified, and 12 inaccurate notification forms were identified. The

inspector observed that over 80 percent of the missed opportunities during the second

quarter 2005 were due to inaccurate emergency notification forms and that over

65 percent of the missed opportunities during the third quarter were because of

inaccurate emergency notification forms with the same errors being made in both

quarters. The inspector noted that the refresher training conducted prior to the job

performance measures as a corrective action for the second quarter performance

deficiencies was only partially successful but did not correct the error rate to historical

facility standards. The inspector concluded that attention to detail errors being made on

the notification forms by the senior licensed operators had increased significantly as

compared to pre-2005 historical performance.

PG&E submitted corrected second quarter PI data on October 21, 2005, as well as the

third quarter PI data. Both quarters indicated the drill and exercise PI as in the White

performance band.

-34- Enclosure

Analysis: The failure to accurately report the drill and exercise performance PI data for

the second calendar quarter of 2005 was a performance deficiency that was more than

minor because it was associated with a cornerstone attribute and affected the

emergency preparedness cornerstone objective (to ensure the adequate protection of

the public health and safety). The finding had human performance cross-cutting

aspects that involved the failure to accurately assess and report the results of evaluated

emergency drills, which, if accurately calculated and reported, would have caused the

NRC to perform an additional inspection in 2005. This issue was not suited for

significance determination process analysis and was evaluated in accordance with

NRCs Enforcement Policy. Supplement 7, Section D.3, to the NRC Enforcement Policy

describes this finding as a Severity Level IV violation.

Enforcement: 10 CFR 50.9 requires, in part, that information provided to the

Commission . . . by a licensee . . . shall be complete and accurate in all material

respects. Contrary to this, PG&E failed to report complete and accurate information for

the second calendar quarter of 2005 and that the drill and exercise performance PI had

crossed the threshold from the Green into the White performance band. The

NRC considers errors in PI data reporting that cause a PI to cross the Green-to-White

threshold to be more than minor because such errors have the potential for impacting

the NRCs ability to perform its regulatory function, which was in this case to perform a

supplemental inspection. This Severity Level IV violation is being treated as an NCV,

consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000275;

323/05-05-06, Failure to Accurately Assess and Report Performance Indicator Data).

This violation is in PG&Es CAP as ARs A0648578 and A0648581 and Nonconformance

Reports N0002199 and N0002200. PG&Es corrective actions included correction of the

second quarter 2005 drill and exercise PI data and initiation of a root cause analysis.

.2 Occupational and Public Radiation Safety Cornerstone

a. Inspection Scope

Occupational Radiation Safety Cornerstone

  • Occupational Exposure Control Effectiveness

The inspector reviewed PG&Es documents from October 2004 through

September 2005. The review included corrective action documentation that identified

occurrences in locked high radiation areas (as defined in PG&Es technical

specifications), very high radiation areas (as defined in 10 CFR 20. 003), and unplanned

personnel exposures (as defined in NEI 99-02). Additional records reviewed included

ALARA records and whole body counts of selected individual exposures. The inspector

interviewed PG&E personnel that were accountable for collecting and evaluating the PI

data. In addition, the inspector toured plant areas to verify that high radiation, locked

high radiation, and very high radiation areas were properly controlled. PI definitions and

guidance contained in NEI 99-02, "Regulatory Assessment Indicator Guideline,"

Revision 3, were used to verify the basis in reporting for each data element.

Public Radiation Safety Cornerstone

  • Radiological Effluent Technical Specification/Offsite Dose Calculation Manual

Radiological Effluent Occurrences

-35- Enclosure

The inspector reviewed PG&E documents from October 2004 through September 2005.

PG&E records reviewed included corrective action documentation that identified

occurrences for liquid or gaseous effluent releases that exceeded PI thresholds and

those reported to the NRC. The inspector interviewed PG&E personnel that were

accountable for collecting and evaluating the PI data. PI definitions and guidance

contained in NEI 99-02, "Regulatory Assessment Indicator Guideline," Revision 3, were

used to verify the basis in reporting for each data element.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

The inspectors performed a daily screening of items entered into PG&Es CAP. This

assessment was accomplished by reviewing ARs and event trend reports, and attending

daily operational meetings. The inspectors: (1) verified that equipment, human

performance, and program issues were being identified by PG&E at an appropriate

threshold and that the issues were entered into the CAP; (2) verified that corrective

actions were commensurate with the significance of the issue; and (3) identified

conditions that might warrant additional followup through other baseline inspection

procedures.

b. Findings

No findings of significance were identified.

.2 Selected Issue Follow-up Inspection

a. Inspection Scope

In addition to the routine review, the inspectors selected the one below listed issue for a

more in-depth review. The inspectors considered the following during the review of

PG&Es actions: (1) complete and accurate identification of the problem in a timely

manner; (2) evaluation and disposition of operability/reportability issues;

(3) consideration of extent of condition, generic implications, common cause, and

previous occurrences; (4) classification and prioritization of the resolution of the

problem; (5) identification of root and contributing causes of the problem;

(6) identification of corrective actions; and (7) completion of corrective actions in a timely

manner.

Documents reviewed by the inspectors are listed in the Attachment.

-36- Enclosure

b. Findings

Introduction: The inspectors identified a Green, NCV of 10 CFR Part 50, Criterion XVI,

for the failure to promptly evaluate ECCS check valve back-leakage and identify

appropriate corrective actions to prevent recurrence. Since 2000, Units 1 and 2 have

experienced ECCS check valve back-leakage which provided a pathway for reactor

coolant to enter the safety injection discharge header and accumulators, or the outflow

of accumulator liquid into the safety injection discharge header. Industry experience has

shown that ECCS check valve back-leakage has the potential to cause gas

accumulation in ECCS piping that can lead to gas-binding of ECCS pumps and/or water

hammer of ECCS piping.

Description: The ECCS is designed with at least two check valves in series to isolate

the high pressure reactor coolant system (RCS) from lower pressure ECCS

components. The check valves that are in series from the four loops of the RCS to the

safety injection system are Valves SI-1-8948A/B/C/D (first-off check valves) and

Valves SI-1-8819A/B/C/D (second-off check valves). Valves 8948A-D were 10-inch,

Darling swing check valves, and Valves 8819A-D are 2-inch Rockwell, Y-pattern, piston

check valves.

Beginning in November 1999, PG&E began to observe pressurization of the safety

injection system discharge header on Unit 2. At that time, PG&E staff believed the

pressurization was a result of back-leakage of the first- and second-off check valves for

the safety injection system, although leakage tests of the valves in the previous outage

showed no leakage. Beginning in August 2000, PG&E staff noted that the Unit 1 safety

injection discharge header also began to pressurize. PG&E staff surmised that the

pressurization was the result of back-leakage of the first- and second-off check valves

from the RCS. For both Units 1 and 2, the safety injection discharge header would

pressurize above the accumulator pressure of approximately 650 psig, which would

conclude that back-leakage through the 8948 and 8819 valves was occurring. On

occasions, operators would have to relieve pressure in the safety injection discharge

header to prevent any challenges to the safety injection discharge header relief valve,

which was set at 1750 psig.

The inspectors reviewed industry operating experience associated with ECCS check

valve back-leakage. In particular, NRC Information Notice 97-40, Potential Nitrogen

Accumulation Resulting from Backleakage From Safety Injection Tanks, discussed

nitrogen gas that had come out of solution in low-pressure safety injection systems and

caused water hammers at two plants. The nitrogen gas came from water in the safety

injection tanks that had arrived at the discharge headers of the safety injection systems

due to back-leakage of ECCS check valves. In dealing with the safety injection

discharge header pressurization, PG&E acknowledged in AR A0496806 that there was

industry operation experience regarding ECCS check valve back-leakage and the

potential for gas-binding of pumps and/or water hammer. However, no voiding of ECCS

piping or pumps were found in Units 1 or 2 safety injection discharge headers. PG&E

had also evaluated other industry operating experience in AR A0636984, and it also

covered situations where nitrogen gas could cause voiding in ECCS piping and pumps if

nitrogen-saturated water was allowed into lower pressure piping due to back-leakage of

ECCS check valves. The inspectors observed that there was no current ECCS check

valve back-leakage into the RHR system discharge header for either unit.

-37- Enclosure

Although some maintenance was performed on the ECCS check valves since 2000,

pressurization of the safety injection discharge header was experienced each operating

cycle, on both units, since the first occurrence in 1999/2000. Specifically,

Valves 8948A-D received pressure isolation valve leak testing each refueling outage, as

well as diagnostic testing once every 4th outage. The inspectors found that

Valves 8819A-D have not received diagnostic or any internal inspection since their initial

installment before plant operation. Valves 8819A-D receive pressure isolation valve

leak testing each refueling outage. The inspectors noted that PG&E tested the first- and

second-off ECCS check valves following each outage and the majority of the valves

exhibited zero recorded leakage. On November 29, 2005, at the exit of Refueling

Outage 1R13, PG&E noted in AR A0610421 that the Unit 1 safety injection discharge

header was pressurizing to over 1000 psig. The inspectors observed in the subsequent

days that operators, at times, were venting the safety injection discharge header twice a

shift in order to prevent the pressurization from challenging the safety injection

discharge header relief valve. The inspectors also observed that PG&E staff was

monitoring for voids in the safety injection discharge header piping and no voids were

found. PG&E staff was developing plans to try and seat the first- and/or second-off

check valves between the RCS and the safety injection discharge header in order to

prevent pressurization. PG&E staff was also developing long-term corrective actions to

prevent future safety injection discharge header pressurization.

The inspectors determined that PG&E staff failed to adequately evaluate and develop

corrective actions for implementation to correct the ECCS check valve back-leakage

that continued to pressurize the safety injection discharge headers on both Units 1

and 2. Specifically, the inspectors noted that, in the past, ECCS check valves would

only receive maintenance if their leakage provided a significant burden to operations.

The inspectors also noted that maintenance on ECCS check valves in the past had

addressed ECCS check valve back-leakage issues. Although the majority of ECCS

check valves exhibited zero leakage at the end of refueling outages, both Units 1 and 2

have continued to experience ECCS check valve back-leakage since 2000. In

assessing the corrective actions for ECCS check valves, the inspectors have not

identified were PG&E has evaluated the adequacy of maintenance and testing to

determine the corrective actions needed to address the long-standing issue of ECCS

check valve back-leakage.

Analysis: The performance deficiency associated with this finding involved the failure to

promptly evaluate ECCS check valve back-leakage and identify appropriate corrective

actions to prevent recurrence as required by 10 CFR Part 50, Criterion XVI. The finding

is greater than minor because it is associated with the Mitigating Systems Cornerstone

attribute of equipment performance and affects the associated cornerstone objective to

ensure the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. Using IMC 0609, Significance

Determination Process, Phase 1 Worksheet, the finding is determined to have very low

safety significance because it did not represent an actual loss of safety function,

represent an actual loss of safety function for a single train for greater than the TS

allowed outage time, or screen as potentially risk significant due to seismic, fire,

flooding, or severe weather initiating events. The cause of the finding is related to the

crosscutting element of problem identification and resolution in that PG&E did not

adequately evaluate and implement timely corrective actions to ECCS check valve back-

leakage.

-38- Enclosure

Enforcement: 10 CFR Part 50, Criterion XVI, Corrective Actions, requires, in part, that

measures shall be established to assure that conditions adverse to quality are promptly

identified and corrected. Contrary to this, ECCS check valve back-leakage has existed

on both units since 2000, and PG&E has failed to promptly evaluate and implement

corrective actions for the back-leakage. The ECCS check valve back-leakage added

operator burden and increased the potential for gas voiding of ECCS components. At

this time, PG&E has not been able to accurately determine which valves have back-

leakage and what has caused the leakage. Corrective actions to restore compliance

included verification of ECCS operability, troubleshooting, and evaluation of possible

future actions to prevent ECCS check valve back-leakage. Because this finding is of

very low safety significance and has been entered into PG&Es CAP as ARs A0526037

and A0610421, this violation is being treated as an NCV, consistent with Section VI.A of

the NRC Enforcement Policy: NCV 50-275; 323/05-05-07, Failure to Promptly Evaluate

Emergency Core Cooling System Check Valve Back-leakage and Identify Appropriate

Corrective Actions to Prevent Recurrence.

.3 Semiannual Trend Review

b. Inspection Scope

The inspectors completed a semi-annual trend review of repetitive or closely-related

issues that were documented in action requests, system and component health reports,

quality assurance audits, trend reports, Diablo Canyon Power Plant internal PIs, and

NRC inspection reports to identify trends that might indicate the existence of more

safety-significant issues. The inspectors review consisted of the 6-month period of

July 1 to December 31, 2005. When warranted, some of the samples expanded beyond

those dates to fully assess the issue. The inspectors also reviewed corrective action

program items associated with turbine building high-energy line break (HELB) louvers

and safety-related check valves. The inspectors compared and contrasted their results

with the results contained in PG&Es quarterly trend reports. Corrective actions

associated with a sample of the issues identified in PG&Es trend report were reviewed

for adequacy. Documents reviewed by the inspectors are listed in the attachment.

b. Findings

The inspectors reviewed two equipment reliability trends as part of the semiannual

trending of problem identification and resolution. Specifically, the inspectors reviewed

documents and observed the condition of safety-related check valves and turbine

building HELB louvers. With respect to the turbine building HELB louvers, the

inspectors noticed that the louvers were installed in 1996. In 1998, PG&E staff began to

find the louvers hard to open due to corrosion at the vanes and bearings. At this time, a

preventive maintenance program was developed to ensure the mobility of the louver

vanes. The louvers were required to be able to freely open to relieve pressure from a

main steam line break inside the turbine building in order to prevent potential structural

damage to the building. PG&E staff later determined that the louvers were sticking in

the closed position because of galvanic corrosion. The louver vanes and frame were

constructed of aluminum, and the vane bearings were constructed of copper. The two

dissimilar metals, along with moisture from the marine environment, provided for the

galvanic corrosion.

-39- Enclosure

In 2002, PG&E staff issued a design change to permanently fix the louvers in the open

position for functionality during an HELB. However, during the rainy season, rain would

blow into the turbine building through the open louvers and as much as 100 gallons of

water may accumulate in the turbine building and potentially impact plant equipment

such as the Unit 2 hydrogen seal oil skid. Subsequently, PG&E instituted a temporary

modification in 2003 and 2004 to return some of the louvers on the Unit 2 side of the

turbine building to their original capability to freely open and close, in order to mitigate

the rainwater intrusion into the building. The temporary modification required monthly

surveillance of the louvers to ensure that they would open freely. At the end of the rainy

season the louvers would again be fixed in the open position. In 2005, a design change

replaced the temporary modification but executed the same actions; namely unfixing a

portion of the Unit 2 louvers during the rainy season, instituting the monthly surveillance

of the louvers, and returning them to their fixed open position after the rainy season.

In 2001, PG&E developed Long-Term Plan 2001-S080-015 to address the long-term

issue regarding the louvers and rainwater intrusion. As of December 31, 2005, funding

and work for Long-Term Plan 2001-S080-015 is scheduled for 2008.

The inspectors also reviewed the problem identification and resolution aspects

associated with check valve reliability and maintenance at Diablo Canyon Power Plant.

In AR A0637470, PG&E and other outside industry reviewers noted several areas in the

plant where long-standing check valve reliability issues posed operator burden and/or

reduced safety system operational margin. Examples of such issues include:

  • Unit 2 reactor coolant pump seal leak-off return line failed its local leak rate test

7 times in the last 10 outages (AR A0540712)

  • Centrifugal charging pump recirculation check valve back-leakage

(ARs A0586882, A0597376, and A0615708)

lube oil into the cylinders (ARs A0601386 and A0601388)

The apparent causes of these long-standing check valve issues were the result of a

check valve preventive maintenance program that needed optimization, roles and

responsibilities regarding the check valve program were not clearly defined or

understood, and trending mechanisms and metrics were inconsistent and not reflective

of the check valve problems. PG&E had initiated corrective actions to address each of

these causes.

The inspectors noted that ECCS check valves were another set of check valves that

have historically added operator burden and had the potential to impact safety system

performance. Specifically, the pressure isolation check valves between the reactor

coolant system, the accumulators, and the safety injection system have experienced

back-leakage on both Units 1 and 2 since 1999. A finding associated with the back-

leakage of ECCS check valves is discussed in Section 4OA2.2.

-40- Enclosure

.4 Inservice Inspection

a. Inspection Scope

Section 02.05 of Inspection Procedure 71111.08 requires review of a sample of

problems associated with inservice inspections documented by the licensee in the CAP

for appropriateness of the corrective actions.

The inspectors reviewed nine action requests which dealt with inservice inspection

activities and found that the corrective actions were appropriate. From this review the

inspectors concluded that PG&E had an appropriate threshold for entering issues into

the CAP and has procedures that direct a root cause evaluation when necessary.

PG&E also had an effective program for applying industry operating experience.

b. Findings

No findings of significance were identified.

.5 Emergency Preparedness Annual Sample Review

a. Inspection Scope

The inspector selected 42 action requests for detailed review. The reports were

reviewed to ensure that the full extent of the issues were identified, an appropriate

evaluation was performed, and appropriate corrective actions were specified and

prioritized. The inspector evaluated the condition reports against the requirements of

Procedure OM7.ID1, Problem Identification and Resolution - Action Requests,

Revision 20A; and Emergency Planning Guide EPG 01, Problem Identification,

Revision May 17, 2002.

b. Findings

No findings of significance were identified.

.6 Radiation Protection

a. Inspection Scope

Section 2OS1 evaluated the effectiveness of PG&Es problem identification and

resolution processes regarding access controls to radiologically significant areas and

radiation worker practices. The inspector reviewed corrective action documents for root

cause/apparent cause analysis against PG&Es problem identification and resolution

process.

b. Findings

Section 2OS1 describes an NRC identified finding, which involved the failure to post a

radiation area. The finding was the same as described in NCV 50-275/02-04-02.

-41- Enclosure

.7 PI&R Crosscutting Aspects

Section 1R14 identified a problem identification and resolution crosscutting aspect for

the failure to conduct a circuit isolation plan, which was the repeat of a similar

performance deficiency described in NRC Inspection Report 05000275; 323/2005004.

Section 2OS1 identified a problem identification and resolution crosscutting aspect for

the failure of radiation protection personnel to post a radiation area and the violation was

similar to a violation previously identified in NRC Inspection Report 050000275;

323/2002004.

Section 4OA2.2 identified a problem identification and resolution crosscutting aspect for

the failure of PG&E to adequately evaluate and implement timely corrective actions to

ECCS check valve back-leakage.

4OA3 Event Follow-up (71153)

.1 (Closed) Licensee Event Report 05000323/2005001-00, TS 3.4.10 Not Met During

Pressurizer Safety Valve Surveillance Testing Due to Random Lift Spread

On January 27, 2005, during scheduled testing of Unit 2 pressurizer safety valves,

PG&E identified two of three pressurizer safety valves outside the TS 3.4.10 lift setting

of >2460 and <2510 psig.

In NRC Inspection Report 05000275; 323/2005003, an NRC-identified, Green NCV of

10 CFR Part 50, Criterion XVI, was identified for this issue. PG&E documented the

problem in Nonconformance Report N0002197. No new information that would change

the disposition of this issue was provided in this LER. This LER is closed.

4OA5 Other

.1 TI 2515/160 - Pressurizer Penetration Nozzles and Steam Space Piping Connections in

U.S. Pressurized Water Reactors

a. Inspection Scope

The inspectors reviewed PG&Es actions regarding the inspection and repair associated

with Alloy 82/182/600 material that may have been used in pressurizer penetration

nozzles, steam space piping connections, heads, and shells. Specifically, the inspectors

reviewed PG&Es response to NRC Bulletin 2004-01, Inspection of Alloy 82/182/600

Materials Used in the Fabrication of Pressurizer Penetrations and Steam Space Piping

Connections at Pressurized Water Reactors. PG&E documented in their response to

the bulletin that no Alloy 82/182/600 material was used in the construction or welds of

the Unit 1 pressurizer. PG&E did not commit to, or perform, any nondestruction

examination methods for the Unit 1 pressurizer. PG&E did perform a boric acid

walkdown of the pressurizer, and the inspectors performed an independent boric acid

inspection of pressurizer.

The activities required in TI 2515/160 for Diablo Canyon Power Plant Unit 1 have been

completed. This temporary instruction is closed for Unit 1.

-42- Enclosure

b. Findings

No findings of significance were identified.

.2 TI 2515/150 - Reactor Pressure Vessel Head and Vessel Head Penetration Nozzles

(NRC Order EA-03-009)

a. Inspection Scope

This area was inspected to verify that PG&Es reactor pressure vessel head and vessel

head penetration nozzle inspection activities are implemented in accordance with the

requirements of First Revised NRC Order EA-03-009 (NRC Accession

No. ML040220391) issued on February 20, 2004, and the Relaxation of Requirements

regarding alternate examination coverage for reactor pressure vessel head penetration

nozzles authorized by NRC letter dated October 26, 2005.

The inspectors observed and reviewed PG&Es activities associated with the volumetric

(ultrasonic) examinations of the reactor pressure vessel head and vessel head

penetration nozzles.

The temporary instruction requires the inspectors to provide a qualitative description of

the effectiveness of PG&Es examinations which, at a minimum, would consist of a

response to the following questions with a brief description of inspection scope and

results.

(1) For each of the examination methods used during the outage, was the

examination:

(a) Performed by qualified and knowledgeable personnel?

For the inspector-observed ultrasonic examinations performed on the

penetration nozzles identified in the Table in Section 1R08,

paragraph 02.01.a, above, the inspectors verified the nondestructive

examination certifications of the four personnel who performed those

examinations. Discussions with those examiners during the course of the

examinations allowed the inspectors to determine that the examiners

were well qualified and knowledgeable in that examination method.

(b) Performed in accordance with demonstrated procedures?

The inspectors verified that the examinations were performed in

accordance with the site-specific demonstrated and qualified procedures

and the applicable ASME Code requirements

(c) Able to identify, disposition, and resolve deficiencies?

The inspectors observed that indications identified during the ultrasonic

examinations were dispositioned in accordance with the acceptance

criteria identified in the ASME Code qualified nondestructive examination

procedure used to perform the examinations.

-43- Enclosure

(d) Capable of identifying the primary water stress-corrosion cracking and/or

reactor pressure vessel head corrosion phenomena described in the

Order?

The nondestructive examination personnel and the procedure used to

perform the ultrasonic examinations were qualified (through

demonstration) to detect primary water stress-corrosion cracking and

reactor pressure vessel head corrosion indications.

(2) What was the physical condition of the reactor vessel head (e.g., loose material,

insulation, dirt, boron from other sources, physical layout, viewing obstructions)?

The inspectors were able to view, via remote camera, the physical condition of

the reactor vessel head and concluded that there were no viewing obstructions

that could adversely impact performance of the volumetric examination.

(3) Could small boron deposits, as described in the Bulletin 01-01, be identified and

characterized?

The inspectors did not review the bare metal examination of the reactor vessel

head because that part of Temporary Instruction 2515/150 was performed

earlier.

(4) What material deficiencies (i.e., cracks, corrosion, etc.) were identified that

required repair?

At the time of this inspection, no material deficiencies had been identified that

required repair.

(5) What, if any, impediments to effective examinations, for each of the applied

methods, were identified (e.g., centering rings, insulation, thermal sleeves,

instrumentation, nozzle distortion)?

PG&E submitted, by letter to the NRC dated May 27, 2005, a request for

relaxation of examination coverage requirements because of vessel head

penetration nozzle end geometry. Specifically, the bottom end of these nozzles

are externally threaded, or internally tapered, or both. This nozzle end geometry

makes inspection difficult and would involve increased personnel radiation dose.

PG&E proposed an alternative inspection that was found to be acceptable and

authorized by NRC letter dated October 26, 2005.

The inspectors noted during the observed examinations that actual examination

coverage was greater than initially expected.

(6) What was the basis for the temperatures used in the susceptibility ranking

calculation, were they plant-specific measurements, generic calculations (e.g.,

thermal hydraulic modeling, instrument uncertainties), etc.?

Information pertaining to the susceptibility calculation is contained in NRC

Inspection Report 50-275;323/04-03.

-44- Enclosure

(7) Was the disposition of indications consistent with the guidance provided in

Appendix B of this Temporary Instruction during nonvisual examinations? If not,

was a more restrictive flaw evaluation guidance used?

At the time of this inspection, no material deficiencies had been identified that

required repair.

(8) Did procedures exist to identify potential boric acid leaks from pressure-retaining

components above the reactor pressure vessel head?

The inspectors did not review the examination of pressure-retaining components

above the reactor pressure vessel head.

(9) Did the licensee perform appropriate follow-on examinations for indications of

boric acid leaks from pressure-retaining components above the reactor pressure

vessel head?

The inspectors did not review the examination of pressure-retaining components

above the reactor vessel head.

This completes the inspection activities required in Temporary Instruction 2515/150,

Revision 3, and this Temporary Instruction is closed with respect to Diablo Canyon

Power Plant Unit 1 (50-275).

b. Findings

No findings of significance were identified.

40A6 Management Meetings

Exit Meeting Summary

On October 20, 2005, the inspectors presented the results of the emergency

preparedness inspection results to Mr. J. Purkis, Acting Station Director, and other

members of his staff who acknowledged the findings.

On November 11, 2005, the inspectors presented the results of the in-service inspection

to Mr. D. Taggart, Manager of Quality Verification Department, and other members of

PG&E staff. PG&E acknowledged the inspection findings.

On November 17, 2005, the inspectors presented the access controls inspection results

to Mr. P. Roller, Director, Operations Services, and other members of his staff who

acknowledged the findings.

The resident inspection results were presented on January 12, 2006, to Mr. David

Oatley, Vice President and General Manager, Diablo Canyon Power Plant and other

members of PG&E management. PG&E acknowledged the findings presented.

The inspectors asked PG&E whether any materials examined during the inspection

should be considered proprietary. Proprietary information was reviewed by the

inspectors and left with PG&E at the end of the inspection.

-45- Enclosure

4OA7 Licensee-Identified Violations

The following violations of very low safety significance (Green) were identified by PG&E

and are violations of NRC requirements which meet the criteria of Section VI of the NRC

Enforcement Policy, NUREG-1600, for being dispositioned as NCVs.

measures be established to assure that conditions adverse to quality, such as

failures, malfunctions, deficiencies, deviations, defective material and equipment,

and nonconformances are promptly identified and corrected. Contrary to this, on

November 3, 2005, PG&E staff discovered deformation and web tearing at the

end connection of the I-beam for Pipe Support 1029-9R. The root cause of the

degradation was determined by PG&E to be friction loads with thermal

movement of the piping exceeding the shear resistance of the I-beam end

connection as it was designed. However, in AR A0653829, PG&E identified the

structural maintenance rule walkdowns in 1997 and 2003 as missed

opportunities for identifying the degraded I-beam; even though the degradation

was determined to have existed at that time. Other missed opportunities

included the post-earthquake walkdowns following the Deer Canyon Earthquake

on October 18, 2003, the San Simeon Earthquake on December 23, 2003, and

the Parkfield Earthquake on September 28, 2004. This finding was determined

to be of very low safety significance since Main Steam Lead 4 was determined to

be able to retain its structural integrity as a result of any design basis accident.

Specifically, structural analysis without the I-beam demonstrated little loss of

design margin.

  • A self-revealing noncited violation of TS 5.4.1.a. was identified for the failure to

appropriately implement the procedure for spent fuel pool skimmer filter

replacement. On November 6, 2005, operators restored to service the spent fuel

pool skimmer system using Section 6.3.2 of Procedure OP B-7:III, Spent Fuel

Pool System - Shutdown and Clearing and Filter Replacement, Revision 16.

After completion of the procedure the spent fuel pool level was noted by

watchstanders to be lower than previous readings. PG&E staff later identified

Valve SFS-2-8765 was not fully shut. This finding impacted the Initiating Events

Cornerstone and was considered more than minor using Example 5.a of

IMC 0612. Specifically, Valve SFS-2-8765 was not operated correctly due to the

reach rod operator interfering with the valve body before the valve was fully shut.

Additionally, operators had two opportunities to identify the mispositioning of

Valve SFS-2-8765 but failed to identify the condition. The mis-positioned valve

resulted in a loss of approximately 2600 gallons of water from the spent fuel

pool. The loss of inventory did not cause level to exceed the TS minimum limits.

Therefore, this finding was determined to be of very low safety significance.

ATTACHMENT: SUPPLEMENTAL INFORMATION

-46- Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

PG&E personnel

J. Becker, Vice President - Diablo Canyon Operations and Station Director

S. Chesnut, Director, Engineering Services

S. David, Manager, Operations

J. Fledderman, Director, Site Services

R. Hite, Manager, Radiation Protection

D. Jacobs, Vice President - Nuclear Services

S. Ketelsen, Acting Director, Nuclear Quality, Analysis, and Licensing

M. Lemke, Manager, Emergency Preparedness

D. Oatley, Acting Chief Nuclear Officer

J. Purkis, Director, Maintenance Services

P. Roller, Director, Operations Services

D. Taggart, Manager, Quality Verification

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000275/2005-05-04 URI Assess Failure of Agastat ETR Time-Delay Relays

05000275/2005-05-03 URI Corrective Actions to Prevent Repetitive Failures of

Auxiliary Feedwater Limitorque Valves (Section 1R15)

Opened and Closed

05000275/2005-05-01 NCV Failure to Adequately Assess and Manage Risk

Associated With Startup Transformer 1-1 Maintenance

(Section 1R14)

05000275/2005-05-02 NCV Failure to Properly Implement Procedure for Safety

Injection System Operation (Section 1R14)

050000275; NCV Failure to Post a Radiation Area (Section 2OS1)

323/2005-05-05

050000275; NCV Failure to Accurately Assess and Report Performance

323/2005-05-06 Indicator Data (Section 4OA1)

050000275; NCV Failure to Promptly Correct Emergency Core Cooling

323/2005-05-07 System Check Valve Back-Leakage (Section 4OA2.2)

A-1 Attachment

Closed

05000323/2005001-00 LER Technical Specification 3.4.10 Not Met During Pressurizer

Safety Valve Surveillance Testing Due to Random Lift

Spread

LIST OF DOCUMENTS REVIEWED

Section 1R05: Fire Protection

Documents

AR PK10-10, Fire Detected, Revision 13

OP -2C, Fire Protection Computer Operation and Response Procedure, Revision 17 and 18

CP 6, Fire, Revision 28

H-5, Containment and Ventilation Systems, Revision 14

Drawings

225054, RCP 1-1 Fire Protection Header, Revision 1

225055, RCP 1-2 Fire Protection Header, Revision 2

225056, RCP 1-3 Fire Protection Header, Revision 1

225057, RCP 1-4 Fire Protection Header, Revision 1

504472, Area F Oil Drip Pan Locations, Revision 6

504473, Area G Oil Drip Pan Locations, Revision 7

Action Requests

A0504285 A0647847

Section 1R06: Flood Protection (71111.06)

Action Requests

A0503193 A0503272 A0503276 A0505617 A0514634 A0563252

A0563325 A0594436 A0595233 A0597321 A0628776 A0628908

A0635208 A0635209 A0639615 A0638953 A0646852

Other Documents

Quality Evaluation Q0012233, Turbine Building Louvers Issues

Long Term Plan 2001-S080-015, Redesign and Replace Turbine Building HELB Louvers,

Units 1 and 2"

A-2 Attachment

Section 1R08: Inservice Inspection Activities (71111.08)

Procedures

Number Title Revision

ER1.ID2 Boric Acid Corrosion Control Program 1

ISI ADD Inservice Inspection Procedure, Additional and Successive 1

SUCCESS Inspections

NDE ET-7 Eddy Current Examination of Steam Generator Tubing 7

NDE PT-1 Solvent Removable Visible Dye Liquid Penetrant Examination 1

Procedure

NDE RT-1 ASME Code Radiography Procedure 8

STP M-SGT1 Steam Generator Tube Inspection 11

TQ1.ID12 Qualification and Certification of NDE Personnel 2

WDI-ET-003 Intraspect Eddy Current Imaging Procedure for Inspection of 8

Reactor Vessel Head Penetrations

WDI-UT-010 Intraspect Ultrasonic Procedure for Inspection of Reactor 11, with

Vessel Head Penetrations, Time of Flight Ultrasonic, FCN01

Longitudinal Wave and Shear Wave

WDP-9.2 Qualification and Certification of Personnel in Nondestructive 6

Examination

WPS 51 Welding of P8 Materials With GTAW and/or SMAW, ASME III, 8

Reg. Guide 1.44(b)

Examination Technique Specification Sheets (ETSS)

Diablo Canyon Power Plant ETSS Qualifying EPRI ETSSs

ETSS #1 (Bobbin) 96001.1, 96004.1, 96005.2, 96007.1, 96008.1,

96012.1, 24013.1, and SG-SGDA-02-41

ETSS #2 (Three Coil Plus Point, 20510.1, 20511.1, 21409.1, 21410.1, 96703.1,

except U-bend) 22401.1, and 22842.3

A-3 Attachment

ETSS #3 (Three Coil Plus Point, 96511.2 and 21409.1

U-bend)

ETSS #4 (Three Coil Plus Point, 99997.1

U-bend High Frequency)

Action Requests

AO 649000 AO 649207 AO 649959

AO 649034 AO 649209 AO 650434

AO 649207 AO 649215 AO 650500

Work Orders

WO C0197316/04 - ASME Code Section III, Class 2, Install New ECCS Suction Void Header

and Associated Piping and Valves

Miscellaneous

Training and testing qualification/certification packages for NDE personnel

Document 51-1264530-12, Diablo Canyon EPRI Appendix H Eddy Current Site Validation,

dated November 2, 2005

EPRI Technical Report 1007904, Steam Generator In Situ Pressure Test Guidelines, Revision 2

Steam Generator Degradation Assessment for Diablo Canyon Unit 1 Refueling Outage 1R13

October 2005, Revision 0, dated 10-28-05

Technical Specification 5.5.9, revised in Amendment 182 to Facility Operating License DPR-80

(Unit 1) and Amendment 184 to Facility Operating License DPR-82 (Unit 2)

Letter from W. Rice to J. Portney, "Pacific Gas and Electric Company Diablo Canyon Units 1

and 2, Pressurizer Weld Material for Unit 1," December 19, 2003

Design Calculation -289, "Calculate Effective Degradation Years for Reactor Heads to Determine

Examination Requirements," Revision 1

PG&E Letter DCL-05-067, "Relaxation Request for NRC Issuance of First Revised Order

(EA-03-009) Establishing Interim Inspection Requirements for Reactor Pressure Vessel Heads at

Pressurized Water Reactors," May 27, 2005

October 26, 2005, NRC Letter to D. H. Oatley, Diablo Canyon Power Plant, Unit No. 1 -

Relaxation of Requirements Associated with First Revised Order (EA-03-009) dated February 20,

2004, Regarding Alternate Examination Coverage for Reactor Pressure Vessel Head Penetration

Nozzles (TAC No. MC7071)

Eddy Current Qualification Record, Site Specific Performance Demonstration for Eddy Current

Analysis of Steam Generator Tubing - November 2005, for the 85 eddy current analysts on site

A-4 Attachment

Section 1R12: Maintenance Effectiveness (71111.12)

Action Requests

A0647478 A0647480 A0647811 A0648515

A0648533 A0648727 A0649118

Other Documents

Procedure MA1.ID17, Maintenance Rule Monitoring Program, Revision 15

Procedure AD7, Work Control, Revision 2

Drawing 102036, Reactor Seismic Trip System, Revision 95

Section 1R13: Maintenance Risk Assessments and Emergent Work Control (71111.13)

Action Requests

A0648949 A0648950 A0648952 A0650443

A0652959 A0653884 A0653953

Work Orders

C0195685

Section 1R14: Operator Performance During Nonroutine Evolutions and Events (71111.14)

Action Requests

A0644160 A0652421 A0653564

Procedures

AD7.DC8, Work Control, Revision 20

MA1.DC11, Risk Assessment, Revision 5A

OP B-3B:I, Accumulators- Fill and Pressurize, Revision 23

Section 1R15: Operability Evaluations (71111.15)

Action Requests

A0639938 A0641553 A0643132 A0644041 A0646914 A0649118

A0649293 A0647625 A0655600

Drawings

107708, Centrifugal Charging Pump 2-2 Lube Oil & Gear Oil Piping, Revision 84

A-5 Attachment

Other Documents

Diablo Canyon Operability Evaluation Log Number 2005-251

Nonconformance Report N0002201

Section 1R19: Postmaintenance Testing (71111.19)

Action Requests

A0650404 A0652664 A0652942 A0655870

Procedures

STP M-11B, Station Battery Condition Monitoring, Revision 25

STP M-12A, Vital Station Battery Modified Performance Test, Revision 14

TQ2.ID4, Training Program Implementation, Revision 8

Work Orders

C0194440 C0198349 C0201145 R0259657

Section 1EP3: Emergency Response Organization Augmentation Testing (71114.03)

Procedures

TQ1, Personnel Training and Qualification, Revision 3

TQ1.ID3, Non-accreditied Training Program Management, Revision 5

OM10.ID4, ERO Management, Revision 7

OM10.DC2, ERO On-Call, Revision 4

Other Documents

Emergency Preparedness Program of Instruction, Revision 11

Section 1EP5: Correction of Emergency Preparedness Weaknesses and Deficiencies

(71114.05)

Action Requests

A0580115 A0613085 A0616080 A0620097 A0620357 A0620468

A0631130 A0631196 A0632271 A0632697 A0632846 A0632991

A0634215 A0634219 A0634256 A0634259 A0634357 A0634611

A0634615 A0634630 A0634635 A0635338 A0635418 A0635423

A0637082 A0637084 A0638648 A0638761 A0638764 A0638766

A0640630 A0641643 A0642334 A0642429 A0645720 A0646245

A0646274 A0646316 A0646830 A0647271 A0648069 A0648572

Nonconformance Reports

N0002199, ERO Drill/Exercise Performance Not Meeting Station Goals, 10/13/2005.

N0002200, Inaccurate EP Drill/Exercise Performance Indicator Data, 10/21/2005.

A-6 Attachment

Procedures

OM10.ID1, Maintaining Emergency Preparedness, Revision 5

OM10.ID2, Emergency Plan Revision and Review, Revision 9

AWP EP-004, 10 CFR 50.54(q) Guidance, Revision 1

AWP EP-005, Determining Compensatory Measures for Equipment Affecting the Implementation

of the DCPP Emergency Plan, Revision 0

Self-Assessment Reports

Interim Compensatory Measures 1st Quarter 2005 Tabletop Drill

Charlie Team 3/12/2005 Rapid Response Tabletop Drill

Bravo Team 2nd Quarter 2005 Health Physics Drill

EPSA 2004-1, Self Assessment of Emergency Action and Classification Levels

EPSA 2004-2, Self Assessment of Palo Verde June 14, 2004 Event

Quality Assurance Assessments

Assessment No. 050200005, 2005 50.54(t) Audit

Quality Performance Assessment Reports

QPAR (2nd Period) June 1 - October 24, 2004

QPAR (3rd Period) October 25 - December 31, 2004

QPAR (1st Period) January 1 - March 31, 2005

QPAR (2nd Period) April 1 - June 30, 2005

Section 2OS1: Access Controls to Radiologically Significant Areas (71121.01)

Corrective Action Documents

A0622516, A0622930, A0624274, A0638745, A0646778, A0649943, A0649193, A0649226,

A0649316, A0649325

Audits and Self-Assessments

Quality Performance Assessment Reports: Third Period 2004, First Period 2005, Second

Period 2005

2R12 Radiation Protection Assessment Report

Radiation Work Permits

05-0010 Operations Activities

05-1031 1R13 Regen HX Room Work

05-1042 1R13 Primary SG Manway Work

05-1050 1R13 RCP Pump Maintenance

A-7 Attachment

Procedures

RCP D-211 Control of Work in Radiologically Significant Areas, Revision 2

RCP D-220 Control of Access to High, Locked High, and Very High Radiation Areas,

Revision 31

RCP D-240 Radiological Posting, Revision 16

RCP D-500 Routine and Job Coverage Surveys, Revision 21

Section 4OA1: Performance Indicator Verification (71151)

Procedures

AWP O-003, NRC Performance Indicators: Occupational Exposure Control Effectiveness,

Revision 3

OM10.DC1, Emergency Preparedness Drills and Exercises, Revision2A

AWP EP-001, Emergency Preparedness Performance Indicators, Revision 5

EP G-3, Emergency Notification of Off-Site Agencies, Revision 43, Attachment 6.1, Instructions

for the DCPP Emergency Notification Form

EP R-2, Release of Airborne Radioactive Materials Initial Assessment, Revision 23

EP RB-10, Protective Action Recommendations, Revision 11

Other Documents

2005 Emergency Drill Schedule

Medical Services/ Evacuee Monitoring/Decontamination May 17-19, 2005

Annual Medical Drill, May 19, 2005

Alpha Team Dress Rehearsal, September 22, 2004

Alpha Team 2004 Plume Phase Ingestion Pathway Exercise, December 8, 2004

Section 4OA2: Identification and Resolution of Problems (71152)

Action Requests

A0496806 A0513448 A0526037 A0528837 A0559173 A0587674

A0609629 A0609710 A0610421 A0610937 A0636258 A0636984

A0637470 A0641418 A0653564 A0653644 A0654587 A0654716

Drawings

047284, Piping Specification S2", Revision 16

106709 - Sheet 2, Safety Injection, Revision 44

A-8 Attachment

Procedures

PEP V-PIV, Cumulative RCS Pressure Isolation Valve (PIV) Leakage, Revisions 0 and 1

TP TB-0522, Determination of Leak Path for SI Header Pressurization, Revision 0

Other Documents

Operational Decision Making Report, Unit 1 Safety Injection pump discharge header pressure is

increasing above accumulator pressure, dated November 30 and December 21, 2005

LIST OF ACRONYMS

ADAMS agency document and management system

AR action request

ASME American Society of Mechanical Engineers

CAP corrective action program

CFR Code of Federal Regulations

EPRI Electric Power Research Institute

ECCS Emergency Core Cooling System

FSAR Final Safety Analysis Report

HELB high-energy line break

IMC Inspection Manual Chapter

LER Licensee Event Report

NCV noncited violation

NEI Nuclear Energy Institute

NRC Nuclear Regulatory Commission

PG&E Pacific Gas and Electric Company

RCS reactor coolant system

RHR residual heat removal

SDP Significance Determination Process

SSC structure, system, and component

TS Technical Specifications

WEXTEX Westinghouse explosive tube expansion

A-9 Attachment