ML053110202

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IR 05000336-05-004, 05000423-05-004; 07/01/2005 - 09/30/2005; Millstone Power Station, Unit 2 and Unit 3; Personnel Performance During Non-Routine Plant Evolutions and Events, Operability Evaluations
ML053110202
Person / Time
Site: Millstone  Dominion icon.png
Issue date: 11/07/2005
From: Paul Krohn
NRC/RGN-I/DRP/PB6
To: Christian D
Dominion Resources
Krohn P, RI/DRP/PB6/610-337-5120
References
IR-05-004
Download: ML053110202 (50)


See also: IR 05000336/2005004

Text

November 7, 2005

Mr. David A. Christian

Sr. Vice President and Chief Nuclear Officer

Dominion Resources

5000 Dominion Boulevard

Glenn Allen, VA 23060-6711

SUBJECT: MILLSTONE POWER STATION UNIT 2 AND UNIT 3 - NRC INTEGRATED

INSPECTION REPORT 05000336/2005004 AND 05000423/2005004

Dear Mr. Christian:

On September 30, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed

inspections at your Millstone Power Station Unit 2 & Unit 3. The enclosed integrated inspection

report documents the inspection findings, which were discussed on October 20, 2005, with

Mr. J. Alan Price and other members of your staff.

The inspections examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report documents two NRC-identified findings of very low safety significance (Green).

One of these findings was determined to involve a violation of NRC requirements. However,

because of the very low safety significance and because it was entered into your corrective

action program, the NRC is treating this issue as Non-Cited Violation (NCV), in accordance with

Section VI.A.1 of the NRCs Enforcement Policy. If you contest these NCVs, you should

provide a response within 30 days of the date of these inspection reports, with the basis for

your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington DC 20555-0001; with copies to the Regional Administrator, Region I; the Director,

Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-

0001; and the NRC Resident Inspector at the Millstone Power Station.

In accordance with 10 CFR 2.390 of the NRC's Rules of Practice, a copy of this letter, its

enclosures, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records component of NRCs

Mr. D. A. Christian 2

document system (ADAMS). ADAMS is accessible from the NRC Website at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Paul G. Krohn, Chief

Projects Branch 6

Division of Reactor Projects

Docket Nos.: 50-336, 50-423

License Nos.: DPR-65, NPF-49

Enclosure: Inspection Report 05000336/2005004 and 05000423/2005004

w/Attachment: Supplemental Information

cc w/encl:

J. A. Price, Site Vice President, Millstone Station

C. L. Funderburk, Director, Nuclear Licensing and Operations Support

D. W. Dodson, Supervisor, Station Licensing

L. M. Cuoco, Senior Counsel

C. Brinkman, Manager, Washington Nuclear Operations

J. Roy, Director of Operations, Massachusetts Municipal Wholesale Electric Company

First Selectmen, Town of Waterford

R. Rubinstein, Waterford Library

B. Sheehan, Co-Chair, NEAC

E. Woollacott, Co-Chair, NEAC

E. Wilds, Director, State of Connecticut SLO Designee

J. Buckingham, Department of Public Utility Control

G. Proios, Suffolk County Planning Dept.

R. Shadis, New England Coalition Staff

G. Winslow, Citizens Regulatory Commission (CRC)

S. Comley, We The People

D. Katz, Citizens Awareness Network (CAN)

R. Bassilakis, CAN

J. M. Block, Attorney, CAN

P. Eddy, Electric Division, Department of Public Service, State of New York

P. Smith, President, New York State Energy Research and Development Authority

J. Spath, SLO Designee, New York State Energy Research and Development Authority

Mr. D. A. Christian 3

Distribution w/encl (VIA E-MAIL):

S. Collins, RA

M. Dapas, DRA

S. Lee, RI OEDO

D. Roberts, NRR

V. Nerses, NRR

G. Wunder, NRR

R. Ennis, NRR

S. Schneider, Senior Resident Inspector

E. Bartels, Resident OA

P. Krohn, RI

S. Barber, RI

ROPreports@nrc.gov

Region I Docket Room (with concurrences)

SISP Review Complete:___PGK_______ (Reviewers Initials)

DOCUMENT NAME: E:\Filenet\ML053110202.wpd

After declaring this document An Official Agency Record it will/will not be released to the Public.

To receive a copy of this document, indicate in the box: C = Copy without attachment/enclosure

E = Copy with attachment/enclosure N = No copy

OFFICE RI/DRP RI/DRP

NAME SSchneider/PGK for PKrohn/PGK

DATE 11/04/05 11/04/05

OFFICIAL RECORD COPY

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket No.: 05000336, 05000423

License No.: DPR-65, NPF-49

Report No.: 05000336/2005004 and 05000423/2005004

Licensee: Dominion Nuclear Connecticut, Inc.

Facility: Millstone Power Station, Unit 2 and Unit 3

Location: P. O. Box 128

Waterford, CT 06385

Dates: July 1, 2005 - September 30, 2005

Inspectors: S. M. Schneider, Senior Resident Inspector, Division of Reactor Projects

(DRP)

J. C. Benjamin, Resident Inspector, DRP

S. R. Kennedy, Resident Inspector, DRP

G. S. Barber, Senior Project Engineer, DRP

A. C. Cerne, Consultant, Division of Reactor Safety (DRS)

L. S. Cheung, Senior Reactor Inspector, DRS

J. M. DAntonio, Operations Engineer, DRS

G. X. Johnson, Reactor Inspector, DRS

G. J. Malone, Resident Inspector-Salem, DRP

T. A. Moslak, Health Physicist, DRS

S. M. Pindale, Senior Reactor Inspector, DRS

D. L. Werkheiser, Reactor Inspector, DRS

Approved by: Paul G. Krohn, Chief

Projects Branch 6

Division of Reactor Projects

Enclosure

CONTENTS

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . iii

REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R01 Adverse Weather Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R04 Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R05 Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

1R06 Flood Protection Measures . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

1R11 Licensed Operator Requalification Program . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

1R12 Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

1R13 Maintenance Risk Assessments and Emergent Work Evaluation . . . . . . . . . . . 7

1R14 Personnel Performance During Non-Routine Plant Evolutions and Events . . . . 8

1R15 Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13

1R16 Operator Work-Arounds . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

1R17 Permanent Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18

1R19 Post-Maintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18

1R20 Refueling and Outage Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

1R22 Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20

1R23 Temporary Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21

1EP6 Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21

RADIATION SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

2PS1 Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems. 2 .2

OTHER ACTIVITIES [OA] . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24

4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24

4OA3 Event Followup . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

4OA4 Cross Cutting Aspects of Findings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28

4OA6 Meetings, Including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 31

SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . A-2

LIST OF DOCUMENTS REVIEWED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-3

LIST OF ACRONYMS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-12

ii Enclosure

SUMMARY OF FINDINGS

IR 05000336/2005-004, 05000423/2005-004; 07/01/2005 - 09/30/2005; Millstone Power

Station, Unit 2 and Unit 3; Personnel Performance During Non-Routine Plant Evolutions and

Events, Operability Evaluations.

The report covered a 3-month period of inspection by resident inspectors and announced

inspections by regional inspectors. One NCV was identified. The significance of most findings

is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply

may be Green or be assigned a severity level after NRC management review. The NRC's

program for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Unit 2

! Green. The inspectors identified a non-cited violation of Technical Specification (TS) 3.8.1.1, AC Sources, since Dominion did not perform the required TS

action (TS 3.8.1.1.b.3) after they discovered the B emergency diesel generator

(EDG) was inoperable on May 18, 2005. Specifically, Dominion failed to verify

that the steam-driven auxiliary feedwater pump was operable after declaring the

B EDG inoperable. In addition, Dominion did not identify in the Licensee Event

Report (LER) documenting this occurrence that TS 3.0.5, Limiting Conditions for

Operation, was also not entered during the time that the B EDG was

inoperable. Dominion has entered this condition into their corrective action

program (CR-05-11468) and updated the LER to reflect TS 3.0.5 applicability.

This finding was more than minor because it affected the human performance

attribute and the availability, reliability, and capability objective of the Mitigating

System cornerstone. Specifically, Dominion did not verify the steam-driven

auxiliary feedwater pump was operable upon the discovery that the B EDG was

inoperable. This finding was determined to be of very low safety significance

(Green) since the steam-driven auxiliary feedwater pump was subsequently

determined to have been available to perform its function. This finding is related

to the cross-cutting area of Human Performance in that operations personnel did

not perform the required actions of TS 3.8.1.1.b.3 after they declared the B

EDG inoperable on May 18, 2005. (Section 1R14.2)

! Green. The inspectors identified a finding where Dominion did not adequately

implement their Operability Determination (OD) procedure on three occasions which

affected the basis for operability for degraded conditions identified on safety-related

systems. Dominion has initiated corrective actions to conduct an assessment of their

iii Enclosure

current operability determination process, evaluate the assessment results, and

implement corrective actions to improve their process. Specifically;

approximately 8 days to evaluate whether a fence installed over the Unit

2 turbine-driven auxiliary feedwater pump (TDAFWP) cubicle high energy

line break blowout panel adversely impacted the panels ability to perform

its design function. After investigation, Dominion determined that a

supporting engineering evaluation did not exist, declared all three

auxiliary feedwater pumps inoperable, and took prompt action to reroute

the fencing around the blowout panel.

charging system when new information discovered during system

troubleshooting showed that the basis for the operability determination

was in question. Dominion ultimately decided to close the operability

determination to previous troubleshooting and maintenance activities

associated with the degraded condition.

  • Dominion described as the basis for operability in a condition report (CR)

that a technical evaluation existed that showed that a Unit 3 high

pressure safety injection (SIH) pump could meet its mission time with an

oil leak of up to six drops per minute. The referenced technical

evaluation however, did not discuss mission time, but calculated the time

to deplete a high pressure safety injection pump oil reservoir in the

presence of a four drop per minute and six drop per minute leak.

This finding was more than minor because it affected the equipment

performance attribute and the availability, reliability, and capability objective of

the Mitigating System cornerstone. Specifically, Dominion did not adequately

evaluate the availability of Mitigating Systems with degraded conditions to ensure

their availability to perform the intended safety function. This finding was

determined to be of very low safety significance (Green) since there was not a

loss of function for the TDAFW and charging system examples and since the

SIH pump would have completed its safety function within the Probabilistic Risk

Assessment 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> evaluation time. This finding is related to the cross-cutting

area of Problem Identification and Resolution (PI&R) because of the failure to

conduct timely and adequate evaluations of degraded and non-conforming

conditions. (Section 1R15)

B. Licensee-Identified Violations

None.

iv Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 2 operated at or near 100 percent power for the duration of the inspection period.

Unit 3 began this inspection period operating at approximately 100 percent power. A manual reactor trip was initiated on September 29, 2005, due to intake structure conditions caused by

high winds and waves which resulted in the trip of both the A and B circulating water pumps.

Due to the proximity of the Unit 3 3R10 refueling outage, Dominion decided to remain

shutdown. The unit was in Mode 4 at the end of this inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01 - One Unit 2 Sample and One Unit 3 Sample)

a. Inspection Scope

System Inspection

The inspectors reviewed one sample each of the readiness of the Unit 2 and Unit 3

service water systems for extreme weather conditions, specifically; hurricanes, high

winds, high tides, ultimate heat sink temperature changes, and other severe weather

events. The inspection was intended to ensure that the indicated equipment, its

instrumentation, and its supporting structures were configured in accordance with

Dominion procedures and that adequate controls were in place to ensure functionality of

the system. The inspectors reviewed licensee procedures and walked down the system.

Documents reviewed during the inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment (71111.04)

a. Inspection Scope

Partial System Walkdowns (71111.04Q - Three Unit 2 Samples and Three Unit 3

Samples)

The inspectors performed six partial system walkdowns during this inspection period.

The inspectors reviewed the documents listed in the Attachment to determine the

correct system alignment. The inspectors conducted a walkdown of each system to

verify that the critical portions of selected systems were correctly aligned in accordance

with these procedures and to identify any discrepancies that may have had an effect on

operability. The inspectors verified that equipment alignment problems that could cause

Enclosure

2

initiating events, impact mitigating system availability or function, or affect barrier

functions were identified and resolved. The following systems were reviewed based on

their risk significance for the given plant configuration:

Unit 2

system during maintenance on the TDAFW system, July 11, 2005;

  • Partial equipment alignment of reactor building closed cooling water (RBCCW),

July 25, 2005; and

  • Partial equipment alignment of A high pressure safety injection (HPSI) train

during an A train protected work week, July 26, 2005.

Unit 3

  • Partial equipment alignment of A train engineered safeguard features air

conditioning, August 13, 2005;

  • Partial equipment alignment of B service water, August 17, 2005; and
  • Partial equipment alignment of the charging pump cooling system, with one

cooling pump (3CCE*P1A) in operation on September 22, 2005, supporting the

operation of two running charging pumps.

b. Findings

No findings of significance were identified.

Complete System Walkdown (71111.04S - One Unit 2 Sample and One Unit 3 Sample)

a. Inspection Scope

Unit 2

The inspectors completed a detailed review of the alignment and condition of the Unit 2

Charging System. The inspectors conducted a walkdown of the system to verify that the

critical portions, such as valve positions, switches, and breakers, were correctly aligned

in accordance with procedures to identify any discrepancies that may have had an effect

on operability.

The inspectors also conducted a review of outstanding maintenance work orders to

verify that the deficiencies did not significantly affect the charging pump system function.

In addition, the inspectors discussed system health with the system engineer and

reviewed the CR database to verify that equipment alignment problems were being

identified and appropriately resolved. Documents reviewed during the inspection are

listed in the Attachment.

Enclosure

3

Unit 3

The inspectors conducted a detailed review, field walkdown, and configuration

inspection of the high pressure safety injection (HPSI) system outside of the

containment building. During normal plant operations, this emergency core cooling

system (ECCS) is in standby, with the charging pump(s) operating as part of the

chemical and volume control system (CVCS). While this inspection was conducted, the

CVCS was configured for maximum letdown flow, in preparation for the upcoming

refueling outage, and two charging pumps were in operation to support the flow

requirements.

The inspectors reviewed the ECCS system design requirements documented in the

Millstone 3 Updated Final Safety Analysis Report and evaluated the field alignment of

the HPSI system components against the system operating procedures and applicable

piping and instrumentation diagram details. The inspectors also examined the

operational readiness of the ECCS equipment, in standby, along the flow path from the

refueling water storage tank. The material condition of the system equipment was

examined and certain components (e.g., snubbers, relief valves) were verified to have

been properly maintained and tested as part of the approved in-service testing program.

All the CRs generated for the CVCS system for the past year were reviewed and a

sample selected for more complete followup of licensee corrective action

implementation. The inspectors examined maintenance work orders and surveillance

test results, and interviewed cognizant operations and engineering personnel, as

necessary, to confirm the adequate implementation of system operability and

programmatic test requirements. Documents reviewed during the inspection are listed

in the Attachment.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

Quarterly Sample Review (71111.05Q - Six Unit 2 Samples and Seven Unit 3 Samples)

a. Inspection Scope

The inspectors performed thirteen walkdowns of fire protection areas during the

inspection period. The inspectors reviewed Dominion's fire protection program to

determine the required fire protection design features, fire area boundaries, and

combustible loading requirements for the selected areas. The inspectors walked down

those areas to assess Dominion's control of transient combustible material and ignition

sources. In addition, the inspectors evaluated the material condition and operational

status of fire detection and suppression capabilities, fire barriers, and any related

compensatory measures. The inspectors then compared the existing conditions of the

inspected fire protection areas to the fire protection program requirements to ensure all

Enclosure

4

program requirements were being met. Documents reviewed during the inspection are

listed in the Attachment. The fire protection areas reviewed included:

Unit 2

  • Auxiliary Building Cable Vault, 25'6" Elevation (Fire Area A-24);
  • A DC Switchgear Room, 14'6" Elevation (Fire Area A-20);
  • B DC Switchgear Room, 14'6" Elevation (Fire Area A-21);
  • 480V Load Center Room, 36'6" Elevation (Fire Area A-28);
  • Auxiliary Building East Battery Room, 14'6" Elevation (Fire Area A-22); and
  • Auxiliary Building West Battery Room, 14'6" Elevation (Fire Area A-23).

Unit 3

  • Electrical Equipment Room, West Switchgear Area, 3'8" Elevation

(Fire Area CB-16);

  • Electrical Equipment Room, East Switchgear Area, 3'8" Elevation

(Fire Area CB-17);

  • Battery Room 1, 3'8" Elevation (Fire Area CB-3);
  • Battery Room 2, 3'8" Elevation (Fire Area CB-4);
  • Battery Room 4, 3'8" Elevation (Fire Area CB-6);
  • Battery Room 5, 3'8" Elevation (Fire Area CB-7); and
  • Auxiliary Building, West Floor Area, 24'-6" Elevation (Fire Area AB-1, Zone D).

b. Findings

No findings of significance were identified.

Annual Fire Drill Observation (71111.05A - One Unit 2 Sample)

a. Inspection Scope

Unit 2

The inspectors observed personnel performance during a fire brigade drill on August 22,

2005, to evaluate the readiness of station personnel to prevent and fight fires. The drill

simulated a fire in the Unit 2 Intake Structure. The inspectors observed the fire brigade

members using protective clothing, turnout gear, and self-contained breathing apparatus

and entering the fire area in a controlled manner. The inspectors also observed the fire

fighting equipment brought to the fire scene to evaluate whether sufficient equipment

was available to effectively control and extinguish the simulated fire. The inspectors

evaluated whether the permanent plant fire hose lines were capable of reaching the fire

area and whether hose usage was adequately simulated. The inspectors observed the

fire fighting directions and communications between fire brigade members. The

inspectors verified that the pre-planned drill scenario was followed and observed the

post-drill critique to evaluate if the drill objectives were satisfied and ensure any drill

weaknesses were discussed.

Enclosure

5

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures (71111.06 - One Unit 3 Sample)

Internal Flooding Inspection

a. Inspection Scope

The inspectors reviewed one sample of flood protection measures for equipment in the

safety-related room listed below. This review was conducted to evaluate Dominions

protection of the enclosed safety-related systems from internal flooding conditions. The

inspectors performed a walkdown of the area and reviewed the FSAR, the internal

flooding evaluation and related documents. The inspectors compared the as-found

equipment and conditions to ensure that they remained consistent with those indicated

in the design basis documentation, flooding mitigation documents, and risk analysis

assumptions. Documents reviewed during the inspection are listed in the Attachment.

Unit 3

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program (71111.11)

.1 Requalification Activities Review by Resident Staff (71111.11Q - One Unit 2 Sample and

One Unit 3 Sample)

a. Inspection Scope

The inspectors observed one sample of Unit 2 licensed operator requalification training

on August 24, 2005 and one sample of Unit 3 licensed operator requalification training

on August 24, 2005. The inspectors verified that the training evaluators ensured

applicable training objectives had been achieved. The inspectors reviewed Unit 2

Training Feedback 2005-00000024 which addressed the operator response to the

change in radiation monitor re-modeling. The inspectors also verified the Appendix R

modification to install control lockout switches in the Unit 3 control room was replicated

in the Unit 3 simulator. Documents reviewed during the inspection are listed in the

Attachment.

b. Findings

No findings of significance were identified.

Enclosure

6

.2 Biennial Review by Regional Specialist (71111.11B - One Unit 3 Sample)

a. Inspection Scope

The following inspection activities were performed using NUREG-1021, Revision 8,

Operator Licensing Examination Standards for Power Reactors, Inspection Procedure

Attachment 71111.11, Licensed Operator Requalification Program, and NRC Manual

Chapter 0609, Appendix I, Operator Requalification Human Performance Significance

Determination Process (SDP), as acceptance criteria.

The inspectors reviewed documentation of operating history since the last requalification

program inspection. The inspectors also discussed facility operating events with the

resident staff. Documents reviewed included NRC inspection reports and eleven

Dominion CRs to ensure that operational events were not indicative of possible training

deficiencies. The inspectors also reviewed Dominion corrective actions and CR

resolutions for issues related to the April 17, 2005 event involving a reactor trip and

inadvertent safety injection. This review included an evaluation of the adequacy of

training conducted to remedy deficiencies in operator knowledge and performance

ascertained from review of the event and verification that all operators had received

the training.

The inspectors observed the administration of operating examinations to one crew.

The operating examination consisted of two simulator scenarios and one set of five job

performance measures administered to each individual.

On September 28, 2005, the inspectors conducted an in-office review of the Dominion

requalification exam results. These results included the annual operating test only

(i.e., the comprehensive written exam was administered last year). The inspection

assessed whether pass rates were consistent with the guidance of NRC Manual

Chapter 0609, Appendix I, Operator Requalification Human Performance Significance

Determination Process. The inspectors verified that:

  • Crew failure rate on the dynamic simulator was less than 20 percent. (Failure

rate was 0 percent.)

  • Individual failure rate on the dynamic simulator test was less than or equal to

20 percent. (Failure rate was 0 percent.)

  • Individual failure rate on the walk-through test (JPMs) was less than or equal to

20 percent. (Failure rate was 2 percent.)

  • Individual failure rate on the comprehensive biennial written exam was less than

or equal to 20 percent. (N/A - this exam was not administered this exam cycle)

  • More than 75 percent of the individuals passed all portions of the exam

(98 percent of the individuals passed all portions of the exam).

Enclosure

7

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12 - Two Unit 2 Samples and Two Unit 3 Samples)

Routine Maintenance Effectiveness Inspection (71111.12Q)

a. Inspection Scope

The inspectors reviewed four samples of Dominion's evaluation of degraded conditions,

involving safety related structures, systems and/or components for maintenance

effectiveness during this inspection period. The inspectors reviewed licensee

implementation of the Maintenance Rule (MR), 10 CFR 50.65, and verified that the

conditions associated with the referenced CRs were appropriately evaluated against

applicable MR functional failure criteria as found in licensee scoping documents and

procedures. The inspectors also discussed these issues with the system engineers and

maintenance rule coordinators to verify that they were appropriately tracked against

each system's performance criteria and that the systems were appropriately classified in

accordance with MR implementation guidance. Documents reviewed during the

inspection are listed in the Attachment. The following conditions were reviewed:

Unit 2

  • Multiple Charging Pump Low Pressure Trip Signal (CR-05-07933); and
  • Degraded A ESF Room Cooler (CR-05-08546).

Unit 3

  • FME Discovered in 3HVQ*ACU2A (CR-05-08623).

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13 - Five Unit 2

Samples and Four Unit 3 Samples)

a. Inspection Scope

The inspectors reviewed nine samples of the adequacy of maintenance risk

assessments of emergent and planned activities during the inspection period. The

inspectors utilized the Equipment-Out-of-Service quantitative risk assessment tool to

evaluate the risk of the plant configurations and compared the results to Dominion's

stated risk. The inspectors verified that Dominion entered appropriate risk categories

and implemented risk management actions as necessary. Documents reviewed during

Enclosure

8

the inspection are listed in the Attachment. The inspectors verified the conduct and

adequacy of scheduled maintenance risk assessments for plant conditions affected by

the conduct of the following maintenance and testing activities:

Unit 2

  • Risk assessment for scheduled work week beginning July 25, 2005;
  • Risk assessment for scheduled work week beginning August 8, 2005;
  • Risk assessment for scheduled work week beginning August 22, 2005; and
  • Risk assessment for scheduled work week beginning September 12, 2005.

Unit 3

  • Risk assessment for scheduled work week beginning August 22, 2005;
  • Emergent Risk Assessment Following Declaration of the A Service Water Train

Inoperable, August 29, 2005; and

  • Risk assessment for work scheduled on September 21, 2005.

b. Findings

No findings of significance were identified.

1R14 Personnel Performance During Non-Routine Plant Evolutions and Events (71111.14 -

Three Unit 2 Samples (including 2 LERs) and Four Unit 3 Samples)

a. Inspection Scope

The inspectors reviewed seven samples of events that demonstrated personnel

performance in coping with non-routine evolutions and transients. The inspectors

observed operations in the control room and reviewed applicable operating and alarm

response procedures, TSs, plant process computer indications, and control room shift

logs to evaluate the adequacy of Dominion's response to these events. The inspectors

also verified the events were entered into the corrective action program to resolve

identified adverse conditions. The inspectors also evaluated two licensee event reports

(LERs) which described personnel performance issues as a causal factor. Documents

reviewed during the inspection are listed in the Attachment.

Operator Performance During Non-Routine Plant Evolutions and Events

Unit 2

  • On August 4, 2005, control room operators received a Control Element

Assembly (CEA) Motion Inhibit and CEA Group Deviation Backup alarms for

CEA #47 during steady state operating conditions. Control Element

Enclosure

9

Assembly #47 position was erratic for approximately two seconds then returned

to its normal pre-alarming condition. Operators entered abnormal operating

procedure (AOP) 2556, CEA Malfunction, for this condition and entered the

applicable TS limiting condition of operations (LCOs). Operators verified

expected positions of the remaining CEA position indications. In addition, no

changes in reactor power and reactor coolant system temperature were noticed

by the control room personnel. Operators determined that this condition was

only an indication abnormality and not an unexpected CEA movement. The

cause of the alarming CEA condition was determined to be a sticking reed

switch. The CEA was subsequently retested and the applicable TS LCOs

exited. Dominion entered this condition into their corrective action program

(CR-05-08843).

Unit 3

  • On July 5, 2005, Operations personnel responded to a fire in the A generator

leads cooling fan motor, located in the turbine building. The operators secured

the affected A fan motor and started the B fan motor and entered Emergency

Operating Procedure (EOP) 3509, Revision 018-00, Fire Emergency. The fire

brigade was mobilized. The fire was extinguished using a portable carbon

dioxide extinguisher. A fire watch was established and the affected motor was

safety-tagged out. The fire did not affect safety-related equipment and was

extinguished in approximately eleven minutes. Operators walked-down affected

areas with no additional issues identified and the EOP was exited. The cause of

the fire was a phase short in the fan motor winding.

  • On July 13, 2005, Maintenance personnel observed a low freon pressure

condition on the B train air-conditioning unit (3HVQ*ACU1B) that supports the

B train residual heat removal, safety injection, and quench spray systems. The

control room responded and entered the appropriate TSs, maintained the A

train ECCS in a protected line-up, and took actions for an apparent freon leak.

Repairs were completed and normal system line-ups were restored. Additionally,

Dominion took appropriate actions to minimize risk to the plant while the affected

air-conditioning unit was unavailable.

  • On August 3, 2005, Dominion determined that a post-maintenance test (PMT)

activity to conduct a leak rate test following maintenance on a containment

pressure boundary airlock shaft seal had been missed in 2001 and 2003.

Operations personnel conducted a reasonable assurance of continued

operability for containment integrity and determined that the shaft seal was

operable but not fully qualified.

Additionally, Operations personnel entered TS 4.0.3., Surveillance

Requirements, since the Unit 3 TS bases listed 10 CFR 50, Appendix J, "Primary

Reactor Containment Leakage Testing for Water Cooled Power Reactors," as a

condition based surveillance under TS 4.0.3. The inspectors noted that TS 4.0.3

would not require an operability determination, would not apply to a missed PMT

Enclosure

10

activity, and that operability would need to be immediately assessed without

delay. In this circumstance, Operations personnel did assess the immediate

operability issue, concluding that even with the worst case shaft seal leak rates,

the overall containment integrated leakage rate would still be less than the

regulatory limit. Operations personnel, however, considered that TS 4.0.3 still

applied. The inspectors consulted with Nuclear Reactor Regulation technical

staff and determined that TS 4.0.3 would allow a delay in conducting a missed

periodic surveillance activity and that TS 4.0.3 would also assume operability

was not affected by a missed periodic surveillance.

In the circumstances of August 3, 2005, the activity was a missed airlock shaft

seal PMT that was intended to establish operability upon its completion, not a

periodic surveillance activity that had been missed. Missing the PMT was not

more than minor since the overall containment integrated leakage rate,

assuming worst-case seal leakage, remained less than regulatory requirements.

The missed PMT and the action to enter TS 4.0.3 was entered into the licensee's

corrective action program as CR 05-08286, "Missed Surveillance for MPS3

Equipment Hatch."

from 100 percent power in response to a lowering vacuum in the main

condenser. Lowering vacuum in the main condenser occurred after the A and

B circulating water pumps automatically tripped as the result of high traveling

screen differential pressure. Since two circulating water pumps tripped, the main

condenser was isolated and the steam generator atmospheric dump valves were

initially used to remove decay heat and control primary plant temperature. Plant

systems responded as expected and the main condenser was restored

approximately one hour later. Following the reactor trip Unit 3 entered a planned

refueling outage (3R10).

Licensee Event Reports (LERs) Associated With Personnel Performance Issues

Unit 2

.1 (Closed) LER 05000336/2005-001-00, Non Conformance With Surveillance

Requirements

On February 7, 2005, Training personnel discovered that a manual operator on a Unit 2

shutdown cooling total flow control valve was not pinned as intended and required by

Technical Specification (TS) 4.5.2.b, Emergency Core Cooling Systems. This resulted

in the manual operator not being attached to the valve shaft. Dominion installed the pin

correctly and documented the issue in CR-05-01147. The LER was reviewed by the

inspectors and no findings of significance were identified. This LER is closed.

Enclosure

11

.2 (Closed) LER 05000336/2005-003-00, 01, Non-Compliance With Technical

Specifications Due to Installation Of Unqualified Test Equipment

a. Inspection Scope

On May 18, 2005, Operations personnel responded to a non-safety related test

instrument which was discovered installed and connected across the voltage sensing

potential transformer of the Unit 2 B EDG. The subject test instrument was used while

testing the EDG approximately five days earlier. The subject test equipment was not

provided with a qualified isolation device used to provide the necessary separation from

the safety related equipment. Although the test equipment was still installed, the B

EDG was incorrectly declared operable while in Mode 5 on May 13, 2005, following

completion of testing. The LER was reviewed by the inspectors and found that one of

the affected Technical Specification (TS) 3.0.5, Limiting Conditions of Operation, was

not identified in the original LER to add reference to the missed TS entry. The

inspectors interviewed Dominion personnel and reviewed this LER with its associated

CRs (CR-05-05660, CR-05-05517, and CR-05-05884) to verify that the root cause and

corrective actions related to the event described in the LER were adequate. Dominion

revised the LER. In addition, as a result of this review, a Green NCV was developed.

This LER is closed.

b. Findings

Introduction. A Green non-cited violation (NCV) was identified for the failure to

recognize and take action directed by Technical Specification (TS) 3.8.1.1.b.3 upon the

discovery that the B EDG was inoperable.

Description. On May 18, 2005, Dominion determined that the B EDG was incorrectly

declared operable following surveillance testing performed on May 13, 2005.

Restoration efforts following the May 13, 2005, surveillance did not remove a non

safety-related piece of test equipment attached to the B EDG. One of the test

equipment leads was connected across the B EDG voltage sensing potential

transformer. This instrumentation was not provided with a qualified isolation device to

provide the necessary separation from the safety-related B EDG equipment. Dominion

determined that the test equipment was not removed following the surveillance due to

an inadequate shift turnover.

Dominion determined this issue to be reportable under 10 CFR 50.73(a)(2)(i)(B) since

the B EDG was not operable when Dominion entered Mode 4 on May 15, 2005, until

the test equipment was removed and operability restored, on May 18, 2005. Dominion

initially determined that the TSs affected were TS 3.8.1.1 Actions b.1, b.2, and b.3, and

TS Surveillance requirements 4.0.5, 4.8.1.1.1, 4.8.1.1.2.a.2, and 4.4.9.3.1.a.

During the review of the LER, the inspectors identified that Dominion did not verify that

the steam-driven auxiliary feedwater (SDAFW) pump was operable once they

recognized that the B EDG was inoperable on May 18, 2005, as required by TS 3.8.1.1.b.3. Dominion subsequently restored the B EDG operability by removing the

Enclosure

12

test equipment leads from the B EDG approximately 30 minutes after the condition

was discovered.

In addition, the inspectors identified that Dominion did not document a violation of TS 3.0.5, Limiting Conditions for Operation, even though A train equipment was taken out

of service while the B EDG was inoperable. Specifically;

  • On May 17, 2005, in Mode 3, 2-FW-43A failure mode testing occurred which

rendered the A auxiliary feedwater (AFW) pump inoperable.

  • On May 17, 2005, in Mode 3, the A HPSI pump was declared inoperable during

HPSI alignment configuration changes.

Dominion subsequently updated the LER to reflect that they were not in compliance with

TS 3.0.5 in addition to the TSs mentioned in the initial LER. The inspectors determined

that Dominions failure to verify the SDAFW pump was available after they determined

the B EDG was inoperable to be a performance deficiency. In addition, Dominion did

not identify in the LER documenting this occurrence, that TS 3.0.5 was also not entered

during the time that the B EDG was inoperable.

Analysis. Traditional enforcement does not apply for this finding because it did not have

any actual safety consequences or the potential for impacting the NRCs regulatory

function and was not the result of any willful violations of NRC requirements. This

finding was more than minor because it affected the human performance attribute and

the availability, reliability, and capability objective of the Mitigating System cornerstone.

This finding was determined to be of very low safety significance (Green) in accordance

with Inspection Manual Chapter (IMC) 0609, Appendix A, Determining the Significance

of Reactor Inspection Findings for At-Power Situations. Specifically, the SDAFW pump

was subsequently verified to have been operable during the time the B EDG was

unavailable. This finding is related to the cross-cutting area of Human Performance in

that operations personnel failed to perform the required actions of TS 3.8.1.1.b.3 after

they declared the B EDG inoperable on May 18, 2005.

Enforcement. TS 3.8.1.1.b.3, A. C. Sources, requires, in part, that in Modes 1, 2, 3,

and 4, the steam driven AFW pump be verified OPERABLE with one EDG inoperable.

Contrary to this requirement, on May 18, 2005, Dominion did not to take this TS action

with the B EDG inoperable in Mode 1. This issue was determined to be of very low

safety significance (Green) and was entered into Dominions corrective action program

(CR-05-11468). Dominion also updated the LER to reflect TS 3.0.5 applicability. This

violation is being treated as an NCV, consistent with Section VI.A of the NRC

Enforcement Policy (NCV 05000336/2005004-01).

Enclosure

13

1R15 Operability Evaluations (71111.15 - Five Unit 2 Samples and Six Unit 3 Samples)

a. Inspection Scope

The inspectors reviewed eleven operability determinations associated with degraded or

non-conforming conditions to ensure that operability was justified and that mitigating

systems or those affecting barrier integrity remained available and no unrecognized

increase in risk had occurred. The inspectors also reviewed compensatory measures to

ensure that the measures were in place and were appropriately controlled. The

inspectors reviewed licensee performance to ensure all related TS and FSAR

requirements were met. The inspectors reviewed the following degraded or

non-conforming conditions:

Unit 2

  • Thermal Margin/Low Pressure Pre-Trip (CR-05-07988);
  • Reactor Building (RB)-50A/RB-50B Found Out of Position (CR-05-07917);
  • Upper 4160 Switchgear Cooling F-134 Out of Service (CR-05-09337);
  • 2-FW-43B Maintenance (CR-05-05259); and
  • Intermittent A and B Charging System Low Pressure Trip Alarms

(OD MP2-012-05).

Unit 3

  • Degraded Rubber Liner Identified on 3SWP*V040 (CR-05-07099);
  • Equipment Hatch Man-Way Shaft Seals Were Replaced Without a Post

Maintenance Test (CR-05-08272);

  • B EDG 2 Percent Water in Rocker Arm Lube Oil (CR-05-07466);
  • A Service Water Pipe Support Significantly Corroded (CR-05-09162);

(CR-05-09317); and

b. Findings

Unit 2/Unit 3

Introduction. The inspectors identified a finding where Dominion did not adequately

implement their Operability Determination (OD) procedure on three occasions which

affected the basis for operability for degraded conditions identified on safety-related

systems. Specifically;

  • Dominion did not perform a timely assessment of operability when the inspectors

questioned whether a fence installed over the Unit 2 turbine-driven auxiliary

feedwater (TDAFW) pump cubicle high energy line break (HELB) blowout panel

could adversely impact the blowout panels ability to perform its design function.

Enclosure

14

  • Dominion did not evaluate new information that called into question the technical

basis of an OD on the Unit 2 charging system.

  • Dominion indicated that a technical evaluation existed that showed that a Unit 3

safety injection high (SIH) pump could meet its mission time with an oil leak of up

to six drops per minute as a basis for operability. The referenced technical

evaluation, however, did not discuss mission time, but calculated the time to

deplete a SIH pump oil reservoir in the presence of a four drop per minute and

six drop per minute oil leak. In addition, Dominion did not revise this operability

basis when the inspectors identified to Operations that the referenced technical

evaluation did not support the operability basis.

Description. On June 27, 2005, the inspectors identified that a security fence was built

directly over the Unit 2 TDAFW pump cubicle HELB blowout panel. The purpose of this

panel is to prevent a complete loss of the auxiliary feedwater (AFW) function if a steam

rupture were to occur in the TDAFW pump room by allowing the steam to relieve into

the turbine building rather than into the adjacent MDAFW pump room. The inspectors

notified Dominion engineering and operations staff and questioned the operability of the

HELB blowout panel with the security fence installed. The inspectors were informed that

a technical evaluation existed which had evaluated this condition and found it

acceptable. On June 28, June 29, and June 30, 2005, the inspectors requested the

technical evaluation from Dominion engineering staff. On July 5, 2005, Dominion

determined that they were unable to find the technical evaluation and subsequently

declared all three AFW pumps inoperable. Dominion entered TS 3.7.1.2.c, Auxiliary

Feedwater Pumps, and took immediate action to remove the section of fencing installed

over the blowout panel. On August 10, 2005, Dominion issued a technical evaluation

which concluded that the HELB blowout panel would have performed its function with

the security fence installed. Dominion procedure RP-5, Operability Determinations,

Revision 004-01, requires, in part, that Upon notification of a degraded or

non-conforming condition, the Shift Manager must perform an immediate determination

of the impact of the deficiency on the operability or functionality of the SSC [Structure,

System, or Component]. In addition, RP-5 requires that a timely and adequate OD

should be initiated whenever the ability of a SSC to perform its specified safety or

support function is called into question. When the inspectors identified this condition to

Dominion on June 27, 2005, neither operations nor engineering personnel recognized

that the technical evaluation did not exist and that there was a need to determine the

impact of this fence on the operability of the HELB blowout panel and its affect on the

AFW system.

On July 26, 2005, the Unit 2 A charging pump received multiple low pressure trip

alarms in the control room. Operators took action to start and align the non-running

B charging pump to the A train and secured the A charging pump. Dominion

concluded that this condition did not effect operability since the charging low pressure

trip alarm is by-passed on a safety injection actuation signal (CR-05-07933). On

July 29, 2005, at the B charging pump received similar multiple low pressure trip

alarms and operators took action to declare it inoperable. On July 30, 2005, the

Enclosure

15

A charging pump received a brief intermittent low pressure trip alarm which cleared

without additional operator action.

Dominion subsequently performed an OD to provide reasonable assurance that the A

charging pump was operable but not fully qualified. The charging pump is included as

an ECCS subsystem required by TS 3.5.2. An OD was not written to address the B

charging pump which exhibited a similar condition. The cause of the multiple low

pressure alarms was believed to be due to a combined effect of gas in the charging

pumps low pressure trip sensing lines and the failure to have charging pump suction

stabilizer heaters energized. The suction stabilizer heaters were believed to reduce the

peak to peak pressure of the charging positive displacement pumps. To ensure that a

common cause condition did not exist for the C charging pump, a Site Operations

Review Committee (SORC) reviewing this matter recommended venting the C

charging pump shortly after the condition presented itself on the A and B charging

pumps. The inspectors identified that this was not performed until several weeks after

the SORC recommendation. Dominion provided interim compensatory measures to

ensure that periodic venting of the low pressure switches and to perform shiftly checks

to ensure that at least one suction stabilizer remained energized.

On August 30, 2005, during troubleshooting, Dominion determined that the current OD

could not be validated from the actual data obtained from the troubleshooting (i.e., the

air in the instrumentation lines and the suction stabilizer heaters OD basis could no

longer be supported as a basis for operability). On August 31, 2005, the inspectors

questioned Dominion engineering staff on what impact this new information had on the

current charging pump OD. On September 1, 2005, the inspectors discussed the new

information with Dominion operations staff indicating that it appeared that the OD would

need to be revised to address this new information. On September 2, 2005, the

inspectors noted that Dominion engineering and operations staff were aware of the new

information, however, they had not revised the OD nor did they intend to evaluate the

OD for revision until the following week. The inspectors informed Dominion operations

and engineering management who recognized the need to reflect the new information

into the OD basis in a more timely manner. On September 3, 2005, Dominion closed

the OD to actions already taken. When the basis of operability cannot be confirmed,

Dominions OD procedure, RP-5, requires operators to declare the component

inoperable and enter the TS action statement or implement appropriate procedural

guidance. In this circumstance, operators did not declare the component inoperable nor

did they revise the OD to provide a different basis for operability when the new

information called into question the existing basis for operability.

On September 22, 2005, Dominion discovered an oil leak on the A intermediate head

safety injection pump. The leak was determined to be approximately 4 drops per

minute. Dominion determined that this degraded condition did not affect operability.

Dominions basis for this determination was that a previous evaluation (Technical

Evaluation M3-EV-04-0039, Safety Injection Pump Oil Reservoir Volume and Depletion

Time) had determined that the safety injection pump could perform for its designed

mission time with an oil leak of up to six drops per minute. The inspectors reviewed

M3-EV-04-0039 and determined that this technical evaluation established estimated run

Enclosure

16

times for two specific leak rates, however, it did not discuss SIH pump mission time or

whether the SIH pump mission time could be met in the presence of these leak rates.

Dominion has stated that they could not locate an SIH mission time in the design basis

(FSAR), however, the inspectors noted that the SIH system is used in conjunction with

the recirculation spray system and charging systems for the long term recirculation

function. Dominions operability procedure (DNAP 1408) requires an adequate basis

(based on design basis documents and the current licensing basis) to support

operability once a degraded or non-conforming condition is identified. Contrary to this,

operators referenced a technical evaluation that did not support this assertion of SIH

pump operability. In addition, Dominion did not revise this operability basis when the

inspectors pointed out that the subject technical evaluation did not support the

operability basis statements in the CR.

The performance deficiency was that Dominion did not adequately implement their OD

procedure on three separate occasions which affected both Units as described above.

In each circumstance, the operability of safety-related equipment with degraded

conditions was not adequately evaluated and an operability basis was not adequately

defined to ensure the availability of the affected equipment to perform the intended

safety function.

Analysis. Traditional enforcement does not apply for this finding because it did not have

any actual safety consequences or the potential for impacting the NRCs regulatory

function and was not the result of any willful violations of NRC requirements.

This finding was more than minor since it was associated with the mitigating systems

cornerstone attribute of equipment performance and affected the cornerstone objective

to ensure the availability and reliability of systems that respond to initiating events to

prevent undesirable consequences (i.e., core damage). This finding was determined to

be of very low safety significance (Green) for the TDAFW and charging system

examples by using Phase 1 of Inspection Manual Chapter (IMC) 0609, Significance

Determination Process. Specifically, this finding affected only the mitigating systems

cornerstone and did not result in a loss of function per Generic Letter 91-18 once further

evaluation of each condition was conducted.

In addition, a Phase 2 assessment was conducted to determine the significance of the

SIH issue since the SIH pump oil reservoir would have depleted prior to the completion

of the long term recirculation function which is a loss of the design function of the SIH

system. Since the probabilistic risk assessment evaluation time for a Phase 2

assessment was 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and the SIH pump was not expected to fail for approximately

15 days under the oil leak rate value, the Phase 2 assessment determined that the SIH

issue was of very low safety significance (Green). This finding was related to the

Problem Identification and Resolution cross-cutting area because of the failure to

conduct timely and adequate evaluations of degraded and non-conforming conditions.

Enclosure

17

Enforcement. No violation of regulatory requirements occurred. Dominions failure to

adequately implement their OD procedure on three occasions to ensure that the

operability of safety-related equipment with degraded conditions was adequately

evaluated and an operability basis was adequately defined, was considered a Finding of

very low safety significance (Green) (FIN 05000336,423/2005004-02). These issues

have been entered into Dominions corrective action program as CR-05-08141,

CR-05-07367, and CR-05-10257.

1R16 Operator Work-Arounds (71111.16)

.1 Selected Operator Work-arounds (One Unit 2 Sample and One Unit 3 Sample)

a. Inspection Scope

The inspectors reviewed one risk significant operator work-around (OWA) for Unit 2 and

one risk significant OWA for Unit 3 during the inspection period. The inspectors

evaluated the conditions to determine if there were any effects on human reliability in

responding to an initiating event or any adverse effects on the function of mitigating

systems. The work-arounds were also reviewed to ensure compliance with licensee

documents which administratively control OWAs. Documents reviewed during the

inspection are listed in the Attachment.

Unit 2

  • Flanders Line Power Supply

Unit 3

b. Findings

No findings of significance were identified.

.2 Cumulative Effects of Operator Work-Arounds (One Unit 2 Sample and One Unit 3

Sample)

a. Inspection Scope

The inspectors reviewed the current listing of active OWAs for Millstone Unit 2 and

Unit 3. The review was conducted to verify that Dominion procedures and practices

provided the necessary guidance to plant personnel, that the cumulative effects of the

known OWAs were addressed, and that the overall impact on the affected systems was

assessed by Dominion. The inspectors independently assessed the cumulative impact

of known OWAs to determine if they adversely affected the ability of plant operators to

implement emergency procedures, respond to plant transients, or perform normal

functions within the expectations of the established Dominion risk models. In support of

Enclosure

18

this assessment, the inspectors reviewed various CRs regarding OWAs and verified that

OWAs were being identified, tracked, and resolved in Dominion's corrective action

program.

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications (71111.17A - One Unit 3 Sample)

a. Inspection Scope

The inspectors reviewed one sample of a permanent plant modification on Unit 3. The

modification was implemented in June 2005 to resolve a fire protection issue that

spurious hot shorts during a control room fire could potentially open the main steam

pressure relieving bypass valves for more than the analyzed duration of six minutes.

The modification involved adding four two-position switches (one for each valve) to the

control circuitry of the four valves such that a spurious short across the valve open

switch would cause the control fuse to blow instead of opening the affected valve. The

inspectors performed a walkdown of installed switches in the control room and reviewed

the applicable FSAR sections, licensing and design basis documents, calculations,

construction and modification specifications and standards, implementing procedures,

licensee inspection and closeout procedures, contractor and vendor documentation,

seismic, Institute of Electrical and Electronic Engineers and other national standards

and the Dominion 50.59 process. These reviews were conducted to ensure (1) the

modified components, structures and systems remained consistent with the

assumptions indicated in the design basis documents, (2) that system availability,

reliability, functional capability and safety function were maintained, and (3) no

unrecognized conditions that significantly affected risk were introduced into the plant as

a result of the modifications. Documents reviewed during the inspection are listed in the

Attachment.

Unit 3

MOVu74A,B,C,D (DCR M3-04002).

b. Findings

No findings of significance were determined.

1R19 Post-Maintenance Testing (71111.19 - Five Unit 2 Samples and Five Unit 3 Samples)

a. Inspection Scope

The inspectors reviewed ten post-maintenance tests (PMT) samples during this

inspection period. The inspectors reviewed these activities to determine whether the

Enclosure

19

PMT adequately demonstrated that the safety-related function of the equipment was

satisfied given the scope of the work specified and that operability of the system was

restored. In addition, the inspectors evaluated the applicable test acceptance criteria to

verify consistency with the associated design and licensing bases, as well as TS

requirements. The inspectors also verified that conditions adverse to quality were

entered into the corrective action program for resolution. Documents reviewed during

the inspection are listed in the Attachment. The following maintenance activities and

their post-maintenance tests were evaluated:

Unit 2

  • TDAFW Trip Throttle Valve (M2-05-06300);
  • AFW 43B Retest (M2-05-02844);
  • CEA Motion Prohibit Primary Power Supply Replacement (M2-00-14807);
  • Permanently Wire Diagnostic Testing Equipment to the B EDG

(M2-00-08406); and

  • A ESF Air Cooler Cleaning (M2-01-15633).

Unit 3

  • MDAFW Pump Motor Bearing Oil (M3-04-13687);
  • C RPCCW Refurbishment (M3-05-0076);
  • 3SWP*052 Removal/Reinstallation following FME Removal on August 14, 2005

(M3-04-12068); and

  • Containment Equipment Hatch LLRT (M3-05-10794).

b. Findings

No findings of significance were identified.

1R20 Refueling and Outage Activities (71111.20 - 1 Unit 3 Sample)

a. Inspection Scope

Dominion began a Unit 3 refueling outage (3R10) on September 29, 2005. The

inspectors evaluated the outage plan and outage activities to confirm that Dominion had

appropriately considered risk, had developed risk reduction and plant configuration

control methods, had considered mitigation strategies in the event of loss of safety

functions, and had adhered to license and Technical Specification requirements. The

inspectors observed portions of the shutdown and cooldown processes. Additionally,

the inspectors conducted an initial containment walkdown to evaluate the as-found

condition of the containment to ensure no loose material or debris which could be

transported to the containment sump were present. The inspectors verified that

conditions adverse to quality were entered into the corrective action program for

resolution. Inspector activities related to this refueling outage performed after

Enclosure

20

September 30, 2005, will be documented in NRC Inspection Report

05000336,423/2005005. Some of the specific activities observed included:

  • Shutdown Risk Assessment;
  • Shutdown Procedure; and
  • Main Steam Code Safety Valve Surveillance Testing.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22 - Five Unit 2 Samples and Six Unit 3 Samples)

a. Inspection Scope

The inspectors reviewed eleven surveillance activity samples to determine whether the

testing adequately demonstrated equipment operational readiness and the ability to

perform the intended safety-related function. The inspectors attended pre-job briefs;

verified that selected prerequisites and precautions were met; and verified that the tests

were performed in accordance with the procedural steps. Additionally, the inspectors

evaluated the applicable test acceptance criteria to verify consistency with associated

design bases, licensing bases and Technical Specification requirements, and that the

applicable acceptance criteria were satisfied. The inspectors also verified that

conditions adverse to quality were entered into the corrective action program for

resolution. Documents reviewed during the inspection are listed in the Attachment. The

following surveillance activities were evaluated:

Unit 2

  • TDAFW Pump Flow Verification In-Service Testing (SP-2610BO-002);

Unit 3

  • HVQ-ACU2A Flow Test on August 12, 2005 (SP-3628.3);
  • B Recirculation Spray System Containment Isolation Valve Stroke Test (CIV)

(SP-3606.9);

Enclosure

21

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications (71111.23 - One Unit 2 Sample and One Unit 3 Sample)

a. Inspection Scope

The inspectors reviewed two temporary modification samples to verify that the

modifications did not affect the function of important safety systems. The inspectors

reviewed the temporary modifications and their associated 10 CFR 50.59 screening

against the Final Safety Analysis Report and Technical Specifications to ensure the

modifications did not affect system operability or availability. Documents reviewed

during the inspection are listed in the Attachment.

Unit 2

  • A RCP Vibration Monitor (DM2-00-0374-05)

Unit 3

  • Control Building Service Water Enclosure Tube Closure Plate Control Room

Habitability Seal (MP3-05-001)

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness [EP]

1EP6 Drill Evaluation (71114.06 - Two Unit 2 Samples and One Unit 3 Sample)

a. Inspection Scope

The inspectors observed one sample of the conduct of Unit 2 licensed operator

simulator training and one sample of the conduct of Unit 3 licensed operator simulator

training on August 24, 2005. The inspectors evaluated the Operations crew activities

related to evaluating the scenario and making proper classification determinations.

Additionally, the inspectors assessed the ability of Dominions evaluators to adequately

address operator performance deficiencies identified during the exercise.

The inspectors observed one sample of the conduct of Unit 2 licensed operator training

emergency planning drill on July 28, 2005. The inspectors observed the operating crew

performance at the simulator and emergency response organization performance at the

site emergency operations center and technical support center. The inspectors verified

that the classification, notification and protective action recommendations were accurate

and timely. Additionally, the inspectors assessed the ability of Dominions evaluators to

Enclosure

22

adequately address operator performance deficiencies identified during the exercise.

Documents reviewed during the inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

2. RADIATION SAFETY

Cornerstone: Public Radiation Safety [PS]

2PS1 Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems (71122.01

- Ten Unit 2 Samples and Ten Unit 3 Samples)

a. Inspection Scope (10 Samples)

During the period August 29 - September 1, 2005, the inspector conducted the following

activities to verify Dominion was properly maintaining the gaseous and liquid effluent

processing systems to ensure that radiological releases were properly mitigated,

monitored, and evaluated with respect to public exposure. Implementation of these

controls was reviewed against the criteria contained in the 10 CFR Parts 20 and 50,

Dominions Radiological Effluent Monitoring & Offsite Dose Calculation Manual

(REMODCM), and Dominions procedures. This inspection activity represents

completion of ten (10) samples relative to this inspection area.

The inspector reviewed the 2004 Annual Radiological Effluent Release Report to verify

that the effluents program was implemented as required by the REMODCM.

The inspector walked down the major components of the Unit 2 and Unit 3 gaseous and

liquid release systems, with the cognizant system engineers and the Instrument &

Control supervisor, to verify the system configurations complied with the FSAR

description, and to evaluate equipment material condition. Effluent monitors examined

included:

Unit 2

  • RM-8132 - Vent Monitor;
  • RM-8169-1 - Millstone Stack Monitor;
  • CND-RIY-245 - Waste Neutralization Sump;
  • RM-9116 -RB Component Cooling Water;
  • RM-9049 - Clean Liquid Monitor; and
  • RM 9095 - Waste Gas Discharge Monitor.

Enclosure

23

Unit 3

  • HVR-10A/B - Ventilation Vent High & Normal Range Stack Monitor;
  • HVQ-RE49 - Engineered Safeguards Building Ventilation;
  • HVR-19A/B - Millstone Stack via SLCRS High and Normal Range;
  • LWS-RIY70 - Liquid Waste Monitor;
  • DAS-RIY50 - Turbine Building Sump Monitor; and
  • CND-07- Waste Neutralization Sump Monitor;

The inspector observed the implementation of a temporary sampling procedure (OPS-

SP3670, Rev 11-04) that would be used if the supplementary leak collection and release

system monitor (HVR-19B) became inoperable. The inspector attended the pre-job

briefing and observed chemistry technicians taking field samples.

The inspector reviewed the relevant surveillance procedures (SP) and observed

technicians collecting weekly air particulate & iodine samples. Airborne particulate and

iodine samples were taken from the Main Station Stack, using SP-2815, and from the

Unit 2 Enclosure Building roof vent, using SP-2814A.

The inspector reviewed the most current Unit 2 and Unit 3 liquid and gaseous effluent

monitor quarterly functional test results and calibration records to verify that associated

pumps/isolation valves or fans/isolation dampers, respectively, were operable. The

inspector evaluated the current effluent radiation monitor set-point for agreement with

the REMODCM requirements.

The inspector evaluated the preparation of a Unit 3 liquid discharge permit no. 5884, by

observing the technician taking a liquid sample from the Unit 3 B-Waste Test Tank,

using Chemistry Procedure CP-3804A, and preparing the associated records.

The inspector reviewed monthly and quarterly dose projections for liquid and gaseous

effluents performed during the past 12 months to verify that the effluent was processed

and released in accordance with REMODCM requirements.

The inspector reviewed administrative changes made to the REMODCM since

March 11, 2004, to determine if the changes affected Dominions ability to maintain

effluent doses as low as reasonably achievable.

The inspector reviewed monthly, quarterly, and annual dose calculations for calendar

year 2004 through July 2005 to ensure that Dominion properly calculated the offsite

dose from effluent releases and to determine if any performance indicator (criteria

contained in Appendix I to 10 CFR 50) was exceeded.

The inspector reviewed liquid discharge permits for Unit 2 (Nos. 2055, 2054, 2043,

2040) and Unit 3 (Nos. 5819, 5810, 5787, 5777) to evaluate the adequacy of dilution

flow, radioactive content, and overall accuracy of the documented data.

Enclosure

24

The inspector reviewed the air cleaning systems surveillance test results for the high

efficiency particulate and charcoal filtration systems installed in Unit 2 and Unit 3. The

inspector confirmed that the air flow rates were consistent with the FSAR values.

The inspector reviewed the calibration records and quality control records for counting

room instrumentation (Unit 2 detectors - Nos. 2, 3, & 4; Unit 3 detectors - Nos. 11, 12, &

13) used to characterize and quantify effluent samples.

The inspector reviewed the results of Dominions inter-laboratory comparison program

to verify the accuracy of effluent sample analyses performed by Dominion.

The inspector reviewed and discussed with Dominion the validation and verification

results for the effluent software (DOSAIR and DOSLIQ) to ensure the software currently

in use provides accurate dose calculations.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES [OA]

4OA2 Identification and Resolution of Problems (71152)

.1 Daily Review of Problem Identification and Resolution

a. Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems,

and in order to help identify repetitive equipment failures or specific human performance

issues for followup, the inspectors performed a daily screening of items entered into

Dominion's corrective action program. This review was accomplished by reviewing

summary lists of each CR, attending screening meetings, and accessing Dominion's

computerized CR database.

b. Findings

No findings of significance were identified.

Enclosure

25

.2 Annual Sample Review (Two Unit 2 Samples and One Unit 3 Sample)

Unit 2

Main Steam Code Safety Valve Lifting

a. Inspection Scope

The inspectors selected CRs and supporting documents associated with corrective

actions for NCV 05000336/2004007-03, Unit 2 main steam safety valve (MSSV) lift

following uncomplicated turbine trips/reactor trips from 100 percent power. The CR and

CR history was reviewed to ensure that the full extent of the issue was identified, an

appropriate evaluation was performed, and appropriate corrective actions were

specified, prioritized, and implemented. The inspectors evaluated the reports against

the requirements of Dominion's corrective action program. The inspectors reviewed

Dominions engineering analysis, MSSV Lifting Study calculation (S-04129S2), which

was used to model the existing phenomena and investigate solutions. Interviews were

conducted with engineering and operations personnel to assess development and

implementation of corrective actions.

b. Findings and Observations

No findings of significance were identified.

The CRs reviewed were associated with review of events that caused MSSVs to lift from

an uncomplicated trip from 100 percent, their investigation, and corrective actions.

Dominions initial efforts were focused on identifying the cause, which was determined to

be the steam dump system operating at a lower capacity than originally designed.

Dominion performed sensitivity studies and accessed operating experience information

from similar plants. Dominion determined that the most effective corrective action was

to permanently reduce average coolant temperature, which reduced initial steam

generator pressure. Inspector review of Dominions study supported this conclusion.

An adequate corrective action plan was developed and is on schedule to be fully

implemented by the end of Cycle 17 (Fall of 2006) via modification DCR M2-05-001,

which was in draft at the time of this review. For the interim, average coolant

temperature is administratively controlled at the lower end of the existing control band,

which realizes the calculated margin and was verified by reviewing the Shift Turnover

Report. The inspectors noted that the engineering analysis identified additional actions

that had an additive effect to prevent MSSV lift, but were not to be implemented in this

DCR.

Safety Injection Tank (SIT) Leakage

a. Inspection Scope

The inspectors selected CRs and supporting documents associated with corrective

actions for Unit 2 NCV 05000336/2004002-02, Failure to Correct SIT Leakage. The

Enclosure

26

reports were reviewed to ensure that the full extent of the issue was identified, an

appropriate evaluation was performed, and appropriate corrective actions were

specified, prioritized, and implemented. The inspectors evaluated the reports against

the requirements of Dominion's corrective action program. The inspectors also

reviewed operator logs, computer point trend graphs, and selected work orders to

evaluate the present condition of the plant with regard to SIT leakage. Cognizant

engineering and operations personnel were interviewed with respect to the effectiveness

of the implementation of corrective measures.

b. Findings and Observations

No findings of significance were identified.

The initial CR (CR-04-01854) and its apparent cause investigation sufficiently

documented the cause and evaluation of SIT leakage but did not specify corrective

actions to address all elements of the NCV. Dominion identified this deficiency

after initial investigation and management review and initiated an additional CR

(CR-04-06173) to address this issue and supplement corrective actions to

CR-04-01854. The inspectors confirmed continuity of corrective actions between the

two reports and resolution of this deficiency. An adequate corrective action plan was

developed and implemented for SIT leakage and completed during this past refueling

outage (2R16, May 2005). The inspectors noted an improvement in SIT performance

since 2R16 as evidenced by SIT levels and pressure.

Unit 3

Service Water Brazed Joint Leakage

a. Inspection Scope

The inspectors selected CR-04-02255, Entry into Unplanned LCO; Identified Leak from

Service Water Piping in Engineered Safety Feature (ESF); The Leak is coming from

Braze Joint Between 3SWP*V706 and 3SWP*V673, for detailed review. This CR was

associated with service water leakage from a degraded brazed joint of a safety-related

system. The specific CR and CR history were reviewed to ensure that the full extent of

the issues were identified, an appropriate evaluation was performed, and appropriate

corrective actions were specified and prioritized. The inspectors evaluated the reports

against the requirements of Dominion's corrective action program.

b. Findings and Observations

No findings of significance were identified.

Dominions extent of condition involved the full scope of service water leaks and

considered operability, reportability, and previous occurrences. Dominions corrective

actions to date, and those scheduled, appear to be progressing towards replacing all

brazed joints and short-radius service water piping by Cycle 13 (approximately four

Enclosure

27

years from now). Dominion has prioritized their corrective action schedule for significant

replacements with respect to the system affected and whether it is isolable. The

reviewed schedule addresses replacement of the majority of unisolable and ESF service

water connections during the next outage (3R10) with the remaining replacements to

follow over the next three cycles. Overall, the inspectors determined that Dominions

plan to address service water brazed joint leakage is adequate.

.3 Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems

a. Inspection Scope

The inspector reviewed twenty-four (24) CRs, and a Nuclear Oversight Audit of the

REMODCM to evaluate Dominions threshold for identifying, evaluating, and resolving

problems in implementing the effluents control program. This review was conducted

against the criteria contained in 10 CFR Parts 20 and 50, the REMODCM, and the

Dominions procedures.

b. Findings

No findings of significance were identified.

.4 Cross-References to PI&R Findings Documents Elsewhere

Section 1R15 describes a failure to adequately implement the OD procedure on three

separate occasions. In each circumstance, the operability of safety-related equipment

with degraded conditions was not adequately evaluated and an operability basis was not

adequately defined to ensure the availability of the affected equipment to perform the

intended safety function. The finding was related to the cross cutting area of Problem

Identification and Resolution because of the failure to conduct timely and adequate

evaluations of degraded and non-conforming conditions.

4OA3 Event Followup (71153 - One Unit 2 Sample)

(Closed) LER 05000336/2005-002-00, Reactor Coolant System Pressure Boundary

Leakage From Primary Water Stress Corrosion Cracking In A Pressurizer Heater

Sleeve

The inspectors interviewed Dominion personnel and reviewed this LER with its

associated CRs to verify that the root cause and corrective actions related to the event

were adequate. No findings of significance were identified. This LER is closed.

4OA4 Cross Cutting Aspects of Findings

Section 1R14.2 describes a failure to take TS action to ensure that the SDAFW pump

was available when the B EDG was declared inoperable. The finding was related to

the cross cutting area of Human Performance in that operations personnel failed to

Enclosure

28

perform the required actions of TS 3.8.1.1.b.3 after they declared the B EDG

inoperable on May 18, 2005.

4OA5 Other Activities

.1 (Closed) Unresolved Item (URI)05000336/2004008-02, Potential Inoperable Enclosure

Air Conditioner

On December 8, 2004, CR-04-10911 identified a high-pitched whistling noise coming

from the air conditioning (AC) unit that cools the motor control center (MCC) B51

enclosure. On December 9, 2004, the inspectors discussed the corrective actions

planned to address the deficiency with Operations personnel. Dominion informed the

inspectors that the Fix It Now Team would troubleshoot the AC unit and perform

appropriate maintenance. Subsequently, on December 16, 2004, an operator reported

that the unit was whistling and was not providing any cooling to the MCC B51 enclosure.

Dominion declared the MCC B51 inoperable and entered multiple Technical

Specification LCO requirements. The inspectors determined that maintenance was not

performed on this AC unit following identification of the degraded condition on

December 8, 2004. Dominions troubleshooting efforts determined that the freon level in

the system was 50 percent of the full load level as a result of leakage past an AC unit

valve. Dominion repaired the leaking system valve, and recharged the system which

restored operability to MCC B51. An unresolved item (URI) was opened pending NRC

evaluation of Dominions operability determination. On August 10, 2005, Dominion

provided the inspectors with additional information from the AC unit vendor which

concluded that the MCC B51 enclosure AC unit would have operated for at least

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> with two pounds of freon (approximately one-half the normal freon load) and in

consideration of an existing leakrate conservatively assumed to be the amount lost (two

pounds over seven days). As a result, the MCC B51 enclosure AC unit would have

been able to perform its intended safety function. This URI is closed.

.2 (Closed) URI 05000336/2005003-02, Degradation of Turbine-Driven Auxiliary Feedwater

(TDAFW) Pump Cubicle High Energy Line Break (HELB) Protection Function

This URI was opened to assess Dominions evaluation of the impact of a security fence

that was installed over the TDAFW HELB blowout panel. See Section 1R15 for further

discussion. This URI is closed.

.3 (Discussed) URI 05000423/2005003-04, Failure to Formally Disposition Leakage into

the "B" EDG Rocker Arm Lubricating Oil System

Introduction. This URI was opened to assess Dominions response to an abnormal lube

oil sample result for the "B" EDG identified on June 17, 2005, and to follow-up on

Dominions root cause determination and corrective actions. This URI will remain open

pending a review of the ability of the B EDG to meet the intended function given the

conditions discovered on September 27, 2005. Documents reviewed are listed in the

Attachment.

Enclosure

29

Description. On June 17, 2005, Dominion identified that there was 1 percent water in

the main lubricating oil sump of the "B" EDG. On June 18, 2005, Dominion obtained

additional sample results which indicated that the water was actually in the rocker arm

lubricating oil system and was 12.5 percent water content (subsequent analysis

indicated that the water content was closer to 3.2 percent). Operators declared the "B"

EDG inoperable and entered Technical Specification (TS) 3.8.1, AC Sources.

Dominion replaced the rocker arm lubricating oil and restored the "B" EDG to operable

status on June 19, 2005. Dominion verified the water content in the rocker arm

lubricating oil was now between 0.1 percent to 0.2 percent, however, Dominion did not

determine or correct the cause of the leakage nor did Dominion establish a threshold for

water content in the rocker arm lubricating oil beyond which the EDG would be

considered inoperable.

On June 24, 2005, the inspectors met with Operations, Engineering, Condition Based

Monitoring and Licensing personnel. The circumstances of the event and the lack of a

resolution of the cause of the water introduction into the rocker arm lubricating oil were

discussed. The inspectors determined that there was reasonable assurance that the "B"

EDG remained operable with the amount of water that was currently determined to be in

the rocker arm lubricating oil, however, the inspectors did not consider that Dominion

had identified or corrected the cause of the water entry into the rocker arm lubricating oil

nor had they established a water content operability threshold. As a result, the

inspectors initiated a URI pending Dominions completion of a cause analysis and

corrective actions.

On July 6, 2005, the inspectors met with the Station Directors for the monthly Directors

meeting. The inspectors noted to the Directors that the cause of the water leakage into

the rocker arm lube oil had not been identified or corrected and consequently, the

degraded condition had not been formally dispositioned. The inspectors discussed with

the Directors that the basis documented in the condition report did not address the

impact of potential continued water leakage into the rocker arm lubricating oil system on

EDG operability.

On July 11, 2005, the "B" EDG rocker arm lubricating oil results showed an elevated

water content of 2 percent water. Dominion stated in the associated CR that it appeared

that there was a "small cooling water leak" into the rocker arm lubricating oil system.

Dominion identified in the CR that "elevated water content is a long term wear issue of

the rocker arm bearings and does not have an affect on the design function of the

diesel." A Reasonable Expectation of Continued Operability and OD were generated in

which Operations determined the "B" EDG to remain operable. Dominion subsequently

closed the OD because they determined that the EDG was fully qualified. Dominion

continued to trend lubricating oil analysis data but did not initiate further corrective action

to determine the cause of the water entry into the rocker arm lubricating oil, did not

specify any further corrective or compensatory actions while this condition continued to

exist, and did not establish a threshold for water content in the rocker arm lubricating oil

beyond which the EDG would be considered inoperable.

Enclosure

30

On August 2, 2005, the inspectors met with Dominion engineering staff to determine

what Dominion had evaluated as the root cause for this water in-leakage. Dominion

identified that the cause for the water in-leakage was from leaking jacket water O-rings

and that they intended to revise their sampling procedure and review their maintenance

schedule for scheduling corrective action. Dominion also indicated their root cause

investigation was complete. The inspectors continued to follow-up with Dominion during

the month of August to determine what additional actions Dominion intended to take to

monitor this condition and how they intended to evaluate operability in the presence of

this known degraded condition.

On September 13, 2005, the inspectors held a conference call with NRC Technical,

Regional, and Dominion staff to discuss the water in the "B" EDG rocker arm lubricating

oil. The inspectors determined that Dominion did not intend to establish an operability

threshold, compensatory actions, or corrective actions for the elevated water content in

the rocker arm lubricating oil. The inspectors also determined that Dominion was

considering corrective maintenance during the October 2005 outage on the EDG

exhaust cage jumper O-rings which they considered to be the likely source of the

leakage. On September 21, 2005, Dominion subsequently decided to delay corrective

action to replace the exhaust valve cage jumper O-Rings until February of 2006.

On September 27, 2005, Dominion drained the rocker arm lubricating oil reservoir and

replaced the oil with fresh oil in preparation for a surveillance run of the "B" EDG.

Approximately 47 milliliters of water was drained from the reservoir at that time.

Dominion then conducted the monthly operability run for approximately one hour and

sampled the rocker arm lubricating oil at which point a quart of water was drained from

the reservoir (nominal capacity of reservoir is approximately 9 gallons). Dominion

removed the cylinder rocker arm covers and identified water leaking from an exhaust

valve on the Number Seven cylinder head. Dominion declared the "B" EDG inoperable

and initiated a maintenance activity to replace all of the cylinder exhaust valves. The "B"

EDG was restored to service on October 2, 2005.

Dominion determined that four additional cylinders (3-5-6-8) had water leakage similar

to the #7 cylinder. It was noted that the O-rings for the exhaust cages associated with

these cylinders were brittle compared to the O-rings for the cylinders that did not

experience water leakage. Dominion determined that the jacket cooling water that cools

these exhaust valve cages was leaking through the brittle O-rings. This URI will remain

open pending a review of the ability of the B EDG to meet the intended function given

the conditions discovered on September 27, 2005.

.4 Temporary Instruction (TI) 2515/163, Operational Readiness of Offsite Power - Resident

Follow-Up

a. Inspection Scope

The inspectors performed a follow-up inspection of one negative response for

TI 2515/163, Operational Readiness of Offsite Power. The inspectors reviewed the

initial licensee response and interviewed Dominion personnel for additional information.

Enclosure

31

Dominion intends to evaluate future procedure changes to be instituted by the

independent system operator and have documented this in CR 05-09287. This

information was forwarded to Nuclear Reactor Regulation for further review.

b. Findings

No findings of significance were identified.

4OA6 Meetings, Including Exit

TI 2515/163, Operational Readiness of Offsite Power - Resident Follow-Up Exit Meeting

Summary

The inspectors presented the inspection results to Mr. Stephen Scace, Director of

Nuclear Station Safety and Licensing, and other Dominion management on August 24,

2005. Dominion acknowledged the results presented.

Licensed Operator Requalification Program (Biennial) Exit Meeting Summary

The inspector presented the inspection results to members of Dominion management at

the conclusion of the inspection on August 29, 2005, and obtained pass/fail results from

a Dominion representative on September 26, 2005. No materials reviewed were

identified by the licensee as proprietary.

Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems Exit

Meeting Summary

The inspector presented the inspection results to Dominion management on

September 1, 2005. Dominion acknowledged the results presented.

Integrated Report Exit Meeting Summary

On October 20, 2005, the resident inspectors presented the overall inspection results to

Mr. J. Alan Price and other members of his staff who acknowledged the findings. The

inspectors confirmed that proprietary information was not provided or examined during

the inspection.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

D. Aube, System Engineer

K. Beagle, Systems Engineer, Radwaste

G. Belke, Chemistry Technician

N. Bihl, CBM Engineer

G. Blackburn, Nuclear Chemistry, Supervisor of Chemical Processes

R. Bonner, Operations

J. Chadbourne, System Engineer

A. Chyra, PRA Engineer

K. Cortis, IST Engineer

D. Cyr, Senior Nuclear Chemistry Technician - Unit 2

L. Crone, Supervisor, Nuclear Chemistry

D. Dallago, Nuclear Oversight Specialist

G. DAuria, Nuclear Chemistry, Supervisor of Analytical Chemistry

C. DeBiasi, Instrument Technician

J. DiLuna, Engineer, Mechanical Engineering

J. Doroski, Health Physicist

E. Dundon, System Engineer

W. Eakin, Supervisor, Radiological Engineering

W. Gorman, Supervisor, Instrumentation and Control

S. Grondahl, Analytical Chemist

N. Jaycox, Design Engineer

A. Jordan, Director, Nuclear Station Operations & Maintenance

M. Kai, Nuclear Fuels Engineer

B. Krauth, Technical Specialist, Licensing

T. Kulterman, Supervisor of Operator Training

J. Kunze, Operations Manager

J. Laine, Manager, Radiation Protection & Chemistry

L. Lebaron, System Engineer, Unit 3

L. Loomis, System Engineer

W. Mangler, Chemistry Technician

S. Matthess, Nuclear Chemistry, Supervisor of Chemistry Laboratories

T. Morris, Senior Nuclear Chemistry Technician - Unit 3

F. Perkins, MP3 EDG Engineer

T. Pitcher, Chemistry Technician

A. Price, Site Vice President - Millstone

S. Scace, Director, Nuclear Station Safety and Licensing

P. Raimondi, Engineer, Technical Project

S. Turowski, Supervisor, Radiological Technical Support

M. Van Haltern, Nuclear Analysis & Fuels Engineering Supervisor

D. Vining, Systems Engineer, Unit 2

W. Zumbo, Engineer, Electrical and I&C

Attachment

A-2

NRC personnel

G. S. Barber, Senior Project Engineer, Division of Reactor Projects (DRP)

J. C. Benjamin, Resident Inspector, DRP

A. C. Cerne, Consultant, Division of Reactor Safety (DRS)

L. S. Cheung, Senior Reactor Inspector, DRS

J. M. DAntonio, Operations Engineer, DRS

G. X. Johnson, Reactor Inspector, DRS

S. R. Kennedy, Resident Inspector, DRP

G. J. Malone, Resident Inspector-Salem, DRP

T. A. Moslak, Health Physicist, DRS

S. M. Pindale, Senior Reactor Inspector, DRS

S. M. Schneider, Senior Resident Inspector, DRP

D. L. Werkheiser, Reactor Inspector, DRS

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000336/2005004-01 NCV Failure to take TS action with the B EDG

inoperable (1R14.2)

05000336,423/2005004-02 FIN Failure to adequately implement operability

determination procedure on three occasions

(1R15)05000423/2005004-03 NCV Failure to properly correct known water in-

leakage into the B EDG rocker arm

lubricating oil system (4OA5.2)

Closed

05000336/2005-001-00 LER Non Conformance With Surveillance

Requirements (1R14.1)

05000336/2005-002-00 LER Reactor Coolant System Pressure

Boundary Leakage From Primary Water

Stress Corrosion Cracking In A Pressurizer

Heater Sleeve (4OA3)

05000336/2005-003-00, 01 LER Non-Compliance With Technical

Specifications Due to Installation Of

Unqualified Test Equipment (1R14.2)05000336/2004008-02 URI Potential Inoperable Enclosure Air

Conditioner (4OA5.1)05000336/2005003-02 URI Degradation of TDAFW Pump Cubicle

HELB Protection Function (4OA5.2)

Attachment

A-3

Discussed

05000423/2005003-04 URI Failure to Formally Disposition Leakage into

the B EDG Rocker Arm Lubricating Oil

System (4OA5.3)

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

SP-2619A-001, Revision 44-06, Control Room Daily Ultimate Heat Sink Surveillances from

7/20/05 - 8/3/05

Unit 2 Technical Specification

Unit 2 UFSAR

Section 1R04: Equipment Alignment

Partial Equipment Alignment

OP-2308, High Pressure Safety Injection System

SP-2604E, HPSI System Boron Injection Flowpath Verification, Facility 1

SP-2610BO, Revision 000-02, TDAFP and Recirculation Check Valve IST

Drawing 25203-26005, Revision 50, Sheet 3 of 4, Condensate Storage and Auxiliary Feedwater

Drawing 25203-26017, Revision 50, Sheet 1 of 3, Charging System

Drawing 12179-EM-152C-17, Sheet 3 of 3, ESF and MSV Building Ventilation

Drawing 12179-EM-133B, Revision 64, Service Water

FSAR, Section 6.3, Safety Injection System

CR-05-07639, Evidence of RCS Leakage Post 2-SI-247 during HPSI pump surveillances

CR-05-05782, Margin Management Issue 48-HPSI Pump High Flow Testing Margin

OP-3304A, Revision 029-04, Charging and Letdown

OP-3330D, Revision 006-03, Charging Pump Cooling

SP-3604A.1, Revision 013-03, Charging Pump A Operational Readiness Test

SP-3604A.2, Revision 013-06, Charging Pump B Operational Readiness Test

SP-3630D.1, Revision 005-03, Charging Pump Cooling 3 CCE*P1A Operational Readiness

Test

Complete System Alignment

Drawing 25203-26027, Revision 46, Sheet 1 of 4, HVAC System Turbine Building Intake

Structure WHSE and Diesel Generator Rooms

ARP 2590B-046, Revision 000-01, Charging Pump A Trip

ARP 2590B-051, Revision 000-01, Charging Pump B Lube Oil Pressure Lo

ARP 2590B-047, Revision 000-01, Charging Pump A Lube Oil Pressure Lo

ARP 2590B-053, Revision 000-01, Charging Pump C Seal Lube System Pressure Hi/Lo

CR-04-11049, Charging Pump NPSH Questioned by NRC Inspector

Attachment

A-4

CR-04-09268, All 3 Charging Pumps Momentarily Started When Shifting L-1104 From Local to

Remote

CR-05-01702, P18A A Charging Pump Failed Surveillance, Pump Declared Inoperable

CR-05-03126, Recommendations for Managing Charging Dampener Bladder Pressure

CR-05-03713, Low Charging Flow After Starting Pump

CR-05-03945, CRED Required to Repair Charging Support 49,382

CR-05-05489, Unable to Run 3 Charging Pumps Due to Not Able to Achieve 128 gpm Letdown

Flow

CR-05-06739, To Check Charging Pumps Pulsation Dampener Pressure

CR-05-05739, VR-11 Appears to Shift to its Emergency Supply When the A Charging Pump

Starts

CR-05-08140, B Charging Pump Trip Logic Cycled Numerous Times within 7 Minutes

Resulting in Charging Pump Being Made Unavailable

CR-05-08153, I&C Loop Folder Indicate Historical Problems

CR-05-08252, PEO Discovered a Leak on the B Pulsation Dampener

CR-05-08455, The A Charging Pump Discharge Pulsation Dampener Pressure is Below 1700

psig

CR-05-08662, MP2 P18B Charging Pump Reservoir Oil Sample is in the Monitoring Status due

to Ferrous Material

OP-2304E, Revision 015, Charging Pump

AOP 2558, Revision 005, Emergency Boration

SP-2601J-006, Revision 001-13, BA Gravity Feed and Emergency Supply Header Check Part

Stroke IST (Cold Shutdown)

SP-2601J-002, Revision 001-02, Loop 1A and Loop 2A Charging Header Check, Open IST

SP-2601B-001, Revision 020-00, Boric Acid Flow Path Verification

PI&D 104A, Revision 45, Chemical and Volume Control

PI&D 104D, Revision 25, Chemical and Volume Control

PI&D 105A, Revision 20, Charging Pump Sealing and Lubrication

PI&D 113A, Revision 24, High Pressure Safety Injection

Section 1R05: Fire Protection

Millstone Unit 2 Fire Hazards Analysis

FP-EV-99-0002, Expansion Joints in Fire Barriers, Millstone Unit 2

M2-EV-99-0093, MP2 Technical Evaluation Evaluate Compensatory Measures to Use during

Loss of Cooling Ventilation systems Supporting Vital Switchgear Rooms

OP-2315D, Vital Electrical Switchgear Room Cooling systems

CR-05-08071, Pre-job Briefing for Fire Watch not Adequate

CR-05-07653, Lack of Support while Establishing a Continuous Fire Watch

CR-05-04594, Abandoned Continuous Fire Watch Post

CR-04-01783, Some Fire Watches May Not Be Fully Aware of Their Responsibilities

FPI 50-001, Revision 010-00, Fire Brigade Drill Assessment Data Sheet

WC 7, Revision 005, Fire Protection Program

Millstone Unit 3 Fire Hazard Analysis Boundary Drawing

SFP-26, Functional Check of CO2 Fire Protection System

SFP-17, Fire Penetration Seal and Barrier Inspections

Millstone 3, Fire Protection Evaluation Reports, Revision 17

Attachment

A-5

MNPS-3-FSAR

Millstone 3 Fire Hazard Analysis 26

Millstone 3 Fire Hazard Analysis 27

Millstone 3 Fire Hazard Analysis 29

Millstone 3 Fire Hazard Analysis 30

Millstone 3 Fire Hazard Analysis 31

Millstone 3 Fire Hazard Analysis 32

Unit 3 Fire Protection Evaluation Report, Revision 17.3, Auxiliary Building Analysis 5

Unit 3 Technical Requirements Manual, TRM 7.4-1, Fire Related Safe Shutdown Components

Section 1R06: Flood Protection Measures

Calc P) 1072, Service Water Cubicle Flooding Hazards Analysis, Revision 0

Calc P) 1198, Flood Source Termination Evaluation, Revision 0

CR-05-09137, Service Water Pipe Leak

OD-MP3-015-05, Operability Determination for Water Pipe Leak (CR-05-09137)

P&ID 12179-EM-106C, Radioactive Liquid Waste & Aerated Drains

Technical Specification Change # 218 (Amendment 214)

Section 1R11: Licensed Operator Requalification Program

Requalification Activities Review by Resident Staff

AOE-02, Revision 0, Simulator Exam Guide Approval Sheet

AOE-08, Revision 1, Simulator Exam Guide Approval Sheet

Biennial Review by Regional Specialist

CR-05-09253, Operating Exam Malfunction Given Out of Sequence

CR-05-09195. Exam JPM Did Not Function as Planned

CR-05-09236, A Licensed Operator Annual Exam JPM Was Not Reviewed Against the

Simulator Exam for Preconditioning or Double Jeopardy Considerations

MP3 JIT-05-002 MP3 April 17, 2005 Event Review

CR-05-09284, Lessons Learned in Steam Release Events and Operator Training

CR-05-05566, NRC Special Inspection Team Finding - Event Classification

CR-05-03889, Training Department and Operations Review of April 17, 2005 Event

CR-05-05568, NRC Special Inspection Team Finding - EOP Implementation

NTP 122.4, Revision 001-03, Operator Training Branch Examination Security

NTP 144, Revision 003-03, Conducting Simulator Training and Examinations

Section 1R12: Maintenance Effectiveness

System Health Report for Unit 2 Charging System

System Health Report for Unit 2 for A and C ESF Ventilation

System Health Report for Unit 3 B Service Water

System Health Report for Unit 3 for 3HVQ*ACU2A

Attachment

A-6

CR-05-07933, Charging Pump A Cycling On/Off Approximately 2 Times A Second

CR-05-08141, A Charging Pump Tripped Four Times within Approximately One Second

CR-05-08140, B Charging Pump Trip Logic Cycled Numerous Times within 7 Minutes

CR-05-08546, Air Flows Obtained for F15A do not Meet Acceptance Criteria

CR-05-08603, Unplanned LCO Due to Insufficient Service Water through 3HVQ*ACUS2A

CR-05-08623, Foreign Material Found Downstream of Valve SWP*V052

CR-05-08722, B Service Water Pump Failed to Backwash After 4 Hours

CR-05-08769, Multiple Septum Strainer Elements on 2SWP*STR1B Degraded

Section 1R13: Maintenance Risk Assessments and Emergent Work Evaluation

Major Equipment Schedule

Equipment Out of Service Risk Model

CR-05-09162, Unplanned LCO, SW Pipe Support for a 3" Supply in ESF Showing Corrosion

Section 1R14: Personnel Performance During Non-Routine Plant Evolutions and Events

CR-05-01147, 2-SI-306 Manual Operator Appears To Be Not Properly Pinned

CR-05-05660, When Requested To Install Astromed On A Diesel Generator Found Astromed

Installed on B Diesel Generator

CR-05-05517, LS-4590 Terry Turbine Steam Trap Level Switch Malfunctioning

CR-05-05884, LS-4590, Aux FW Turb Water Level Switch, May Require Calibration Check

Following Plant Startup

CR-05-05986, Steam Driven Auxiliary Feed Pump (P4) Steam Supply Water Level Switch

LS-4590 Needs To be Calibrated

CR-05-06075, LS-4590 Terry Turbine Steam Supply Water Detector Level Switch Failure

Mechanism

CR-05-08286, Missed Surveillance for MP3 Equipment Hatch (3CS*HATCH2)

CR-05-08272, O-Rings and V-Rings That Function as Part of the Containment Pressure

Boundary were Inappropriately Downgraded to Non-Safety Related

TS 3.6.1.2, Containment Leakage

TS 4.0.3, Surveillance Requirements

ARP-2590D-053, Revision 000, Aux FW Turb Steam Line Water Level Hi

TS 3/4, Limiting Condition for Operation

TS B3/4.8, Electrical Power Systems

Unit 2 Control Room Logs

Unit 3 Control Room Operations Log, Night Shift, July 06, 2005

CR-05-07458, Need to Schedule Motor Swap for 3GMS-FN1B

CR-05-07423, Vibration Retest for the New 3GMS-FN1A is SAT, but is in Alert

CR-05-07417, Recent Trending of Catastrophic Failures of Motors have Raised concern of the

[sic] our Protective Devices Programs

CR-05-02619, MP3 3GMS-FN1A Fan Motor Vibration is in the Alert Range

CR-05-02909, Retest on 3GMS-FN1A Unsat Due to Vibration Levels Exceeding .66 IPS

CR-05-0750, Low Freon Charge on 3HVQ*ACUS1B

MP-28-AIR-FAP00.2, Revision 001-02, Administration of the Air Quality Management Program

EOP-3509, Revision 018-00, Fire Emergency

Attachment

A-7

OP-3347C, Revision 013-05, Main Transformer and Isophase Bus

OP-3324A, Revision 009-10, Main Generator

Section 1R15: Operability Evaluations

CR-05-07084, Crevice corrosion is identified on the outlet flange face for Unit 3 service water

spool 23-10 (near 3SWP*V040)

CR-05-07091, Degraded coating and rust blooms identified during visual inspection of Unit 3

service water spool 3SWP-23-9 (adjacent to 3SWP*V040)

CR-05-07099, Degraded rubber liner identified on 3SWP*V040

CR-05-07933, A Charging Pump Cycled On/Off Approximately 2 Times a Second

CR-05-08100, PC-224X was Found Air-Bound

CR-05-08124, Emergent Work to Support P18AM Investigation for Operability

CR-05-08140, B Charging Pump Trip Logic Cycled Numerous Times with 7 Minutes

CR-05-08141, A Charging Pump Tripped Four Times with Approximately One Second

CR-05-08153, I&C Loop Folders for PC-224X, PC-224Y, PC-224Z Indicate Historical Problems

CR-05-08163, Fuse Blown for A Charging Stabilizing Heaters

CR-05-07988, Silent TM/LP Pre-Trip Channel A RPS

CR-05-07917, Found 2-RB-50A and 2-RB-50B Out of Required Position

CR-05-08272, O-Rings and V-Rings That Function as Part of the Containment Pressure

Boundary were Inappropriately Downgraded to Non-Safety Related

CR-05-07466, 3EGS*EGB Rocker Arm Oil analyses Results Show Elevated Water Content

CR-05-08769, Multiple Septum Strainer Elements in 3SWP*STR1B Found Degraded

CR-05-09317, Service Water Pipe Leak

CR-05-09162, Unplanned LCO, SW Pipe Support for 3" A Supply in ESF Showing Corrosion

CR-05-09337, Upper 4160V Switchgear Room Temperature 92 Degrees

CR-05-10013, Oil Leakage on 3SIH*P1A 1.25" Oil Drain Line Back to Reservoir from Pump

Inboard Bearing

CR-05-10257, 3SIH*P1A Outboard Pump Bearing Housing is Leaking Oil

CR-04-10084, Oil Found External to the A Safety Injection Pump Oil Line

RP-5, Revision 004-01, Operability Determinations

CE Evaluation dated June 16, 1989, Evaluation of Hot Leg Temperatures

ARP-2590C, Revision 005, Control Room Panel, C-04

MP3 FSAR

MP2 TS, Section 3/4.7, Plant Systems

MP3 TS, Section 3/4.7, Plant Systems

OD MP2-011-05, Operability Determination for TM/LP, CR-05-08050

OD MP2-012-05, A Charging Pump Operability Determination, CR-05-07933

OD MP3-012-05, 3SWP*V040 RECO dated 6/30/05

OD MP3-012-05, 3SWP*V040 Operability Determination, CR-05-07099

OD MP3-014-05, Revision 0, During Review of Bill of Materials for MP3 Equipment Hatch

(3CS*Hatch2) Seal Quality Requirements Identified that the 18" Man-Way Shaft Seals

Replacement During 3R09 Had an Insufficient PMT

OD MP3-016-05, Degraded Service Water Pipe Support 3 SWP-4-PSR248

RECO MP3-014-05, During Review of Bill of Materials for MP3 Equipment Hatch

(3CS*Hatch2) Seal Quality Requirements Identified that the 18" Man-Way Shaft Seals

Replacement During 3R09 Had an Insufficient PMT

Attachment

A-8

RECO/OD MP3-013-05, Lube Oil Analysis For 3 EGS*EGB Rocker Arm Lube Oil Shows An

Elevated Water Content (2%)

RECO MP3-016-05, Degraded Service Water Pipe Support 3 SWP-4-PSR248

RECO MP3-015-05, Service Water Pinhole Pipe Leak in Line 3-SWP-003-324-3

CBM 106, Revision 1, Oil Analysis

AWO M3-05-10794, Perform LLRT on Manway Shaft Seals for Equipment Hatch

MP2-EV-99-0093, Revision 04, Evaluate Compensatory Measures to Use During Loss of

Cooling/Ventilation Systems Supporting Vital Switchgear Room

MP3-EV-05-0001, Revision 2, Estimate of ECCS Hot Leg Recirculation Flow Provided Through

a Seized SIH Pump

MP3-EV-04-0039, Revision 0, Safety Injection Pump Oil Reservoir Volume and Depletion Time

25212-ER-04-0001, Revision 0, Results of ESF Building and Service Water Cubicles Loss of

Ventilation GOTHIC Analysis

M3-04-12068, Install New Valve and Lap Joint IAW DM3-04-0234-04

Section 1R16: Operator Work-Arounds

MP-14-OPS-GDL600, Revision 004-00, Operations Administration Procedures

MP-14-OPS-GDL600, Revision 003-00, Plant Status and Configuration Control

Millstone Station Aggregate Impact Analysis dated 8/1/05

Millstone 2 Weekly Aggregate Impact Assessment Report Dated 8/1/05

Millstone 3 Weekly Aggregate Impact Assessment Report Dated 8/1/05

Millstone 2 & 3 Operator Work-Arounds Management Summary Dated 7/6/05 & 7/29/05

Millstone 2 & 3 Control Panel Issues Management Summary Dated 7/6/05 & 7/29/05

Millstone 2 & 3 Alternate Plant Configurations Management Summary Dated 7/6/05 & 7/29/05

CR-05-07229, 3SWP*STR1C Eagle Reset Timer Discovered Failed During Troubleshooting

CR-05-07228, Received MB4C-1-12, for CVSWP-Z24A, Train A Service Water Pump Strainer

Hasnt Blown Down in 4.5 Hours

CR-05-07749, Momentary Loss 23KV (Flanders Line)

CR-05-07403, Loss of Power from the Flanders Line due to a Blown Disconnect

CR-05-07169, Loss of Flanders Line, Entry into AOP-2508 - Second Trip within 24 Hours

CR-05-07112, Loss of Flanders Line, Entry into AOP-2508

AOP-2508, Revision 000-05, Loss of 23KV Offsite Power

Section 1R17: Permanent Plant Modifications

FP-EV-04-001, Revision 1, 3MMS*MOV74A,B,C and D Control Circuit Hot Short Modification,

Including Lockout Switches

DCN DM3-00-0242-05, Revision 0, DCR M3-04002 Test Plan Enhancements

25212-32001, Sh 6AKM, Elementary Diagram480V MV, MN STM Pressure Relieving Bypass

Valve 3MMS*MOV74B

25212-32001, Sh 6AKP, Elementary Diagram480V MV, MN STM Pressure Relieving Bypass

Valve 3MMS*MOV74D

25212-28036, Sheet 8, Logic Diagram, Turbine Bypass.

WO M3-04-02008, Modify Control Circuit for 3MMS MOVu74A Hot Short Mod

WO M3-04-02009, Modify Control circuit for 3MMS MOVu74B Hot Short Mod

Attachment

A-9

WO M3-04-02009, Modify Control circuit for 3MMS MOVu74C Hot Short Mod

WO M3-04-02009, Modify Control circuit for 3MMS MOVu74D Hot Short Mod

Section 1R19: Post-Maintenance Testing

M2-00-14807, CEA Motion Inhibit Primary Power Supply

M2-05-06300, Main Steam Supply Low-Point Steam Trap

M2-04-08691, Terry Turbine Trip Throttle Valve Rework, July 20, 2005

SP-2610CO-002, Revision 000-01, 2-FW-43A and 2-FW-43B Stroke and Timing IST

SP-2660-002, Revision 004-01, AFP Turbine Trip Throttle Valve Exercise Test

M3-04-13687, Take Oil Samples and Change Oil From MDAFW Motor Bearing, PM 1 Year

U3 TS

U3 FSAR

CR-05-05419, Trip is Blowing By

CR-01-10429, 3FWA-P1B Has An Oil Leak

Section 1R20: Refueling and Outage Activities

OP-3208, Revision 20-13, Plant Cooldown

SP-3712G, Revision 008, Main Steam Code Safety Valve Surveillance Testing (IPTE)

Section 1R22: Surveillance Testing

NRC Inspection Manual 9900, Technical Guidance

SP-2610BO, Revision 000-01, TDAFP and Recirculation Check Valve IST

SP-2402M, Revision 008-16, Functional Test of Steam Generator Level and Auto Aux.

Feedwater Logic

SP-3601F.6, Revision 005-04, Reactor Coolant System Water Inventory Measurement

SP-3622.2-001, Revision 013-02, Auxiliary Feed Pump 3FWA*P1B Operational Readiness Test

SP-3609-001, Revision 012, RSS

SP 3601F.6, Revision 005-04, Reactor Coolant System Water Inventory Measurement

TS 3.7.1.2, Auxiliary Feedwater System

TS 3.3.2, Engineered Safety Features Activation System Instrumentation

TS 3.6.3, Containment Isolation Valves

SR 4.7.1.2, AFW Surveillance Requirement

CR-05-07957, Time Delay Relay 62/Z1 Needs to be Replaced

CR-05-09754, Aux Feed Pump 3FWA*P1B Operations Readiness Test

AWO M2-05-01850, Functional Test of Auto Aux Feedwater Logic

Section 1R23: Temporary Plant Modifications

OP-3225A, Revision 022-01, Circulating Water

WC-10-004, Revision 000-01, Temporary Modification Control Sheet

MP3-05-001, Control Building Service Water Enclosure Tube Closure Plate Control Room

Habitability Seal

Attachment

A-10

Section 1EP6: Drill Evaluation

AOE-02, Revision 0, Simulator Exam Guide (Unit 2 and Unit 3)

DNAP-2605, Revision 1, Drill/Exercise Indicator Performance - NEP

Scenario 1.D., MP2-2

MP-26-EPI-FAP06-002, Revision 003, Emergency Action Levels (Millstone Unit 2)

Section 2PS1: Radioactive Gaseous and Liquid Effluent Treatment and Monitoring

Systems

Procedures:

SP-2815, Revision 001-01, Weekly Main Station Stack, Wide Range Gas Monitor (WRGM)

Sampling for Iodine & Particulates

SP-2814A, Revision 009-02, Gaseous Effluents Sampling for Iodines & Particulates from Unit

2 Vent- Weekly

SP-3614A Series, Unit 3 Auxiliary Building Ventilation System Surveillance Tests

SP-3614I Series, Unit 3 Supplemental Leak Collection & Release System Surveillance Tests

SP-2654Q Series, Unit 2 Containment & Enclosure Building Exhaust Filter L-25 HEPA Filtration

Testing

SP-2609D Series, Unit 2 Enclosure Building Charcoal/HEPA Filtration Testing

VPROC-OPS03-001, Revision 0, In-Place Testing of HEPA Filters & Charcoal Absorbers

SP-3670.1, Revision 11-04, Temporary Sampling Surveillance

SP-3880, Revision 002-01, Unit 3 SLCRS Vent Radiation Monitor Inoperable

Condition Reports:

05-09249, 05-00223, 05-00752, 05-00775, 05-01169, 05-01652, 05-01721, 05-03155,

05-03156, 05-03258, 05-06347, 05-08203, 04-11326, 04-10322, 04-09848, 04-11374,

04-05740, 04-05775, 04-05963, 04-06282, 04-09125, 04-09373, 04-10488, 04-10490

Nuclear Oversight Reports:

Audit 03-11: Offsite Dose Calculation Manual (ODCM) Radiological Environmental Monitoring

(REMP) and Environmental Protection Plan

Section 4OA2: Identification and Resolution of Problems

Main Steam Code Safety Valve Lifting

CR-04-02514, Trending CR for Main Steam Safety Valve Opening After Reactor Trip at

Millstone Unit 2

CR-04-02543, CR Issued for Trending the Lifting of S/G Safety Valves 2-MS-252 and 2-MS-242

Following U2 Reactor Trip on 3/15/04

CR-04-02760, Manual Reactor Tripping Causes SG Safety Valves to Lift

MP2 FSAR, Section 7.4.5.1.1

Attachment

A-11

S-04129S2, MP2 MSSV Lifting Study, dated December 2004

NE-04-F-115, MSSV Lifting Study Results and Recommendation memo, dated December 22,

2004

Millstone Integrated Inspection Report 2004007

RELAP 5 Mod 3.2 Output Summary Graphs, MP2 MSSV Lifting Study

Safety Injection Tank Leakage

NCV05000336/2004002-02, NRC Integrated Inspection Report (Resident)

05000336,423/2004002, dated April 9, 2004

CR-04-01854, Repeated Attempts to Resolve SIT Leakage at Unit 2 is

not Captured Within Level 2 CR Investigation

CR-04-06173, NCV for Untimely Corrective Actions Concerning SIT System Leakage at Unit 2

Requires Additional Actions

Safety Injection Tanks System Health Report, 2005 Qtr. 2

CR-05-06042, OWA-C Operator Distraction Yellow #17, #1 Safety Injection Tank Pressure is

Decreasing

SIT Level Trend Plot for SIT #1-SIT#4, Aug. 2005; dated August 30, 2005

SIT Level Trend Plot for SIT #1-SIT#4, Jan. 2005-April 2005; dated August 30, 2005

SIT Level Trend Plot for SIT #1, May 2005-Aug. 2005; dated August 30, 2005

SIT Pressure Trend Plot for SIT #1-SIT#4, Aug. 2005; dated August 30, 2005

Containment Pressure, SIT #2 PressureTrend Plot, Aug. 2005; dated August 30, 2005

ARP 2590A/A-10, Revision 000-01, Safety Injection Tank 1 Level Hi

ARP 2590A/B-10, Revision 000, Safety Injection Tank 1 Level Lo

ARP 2590A/C-10, Revision 000, Safety Injection Tank 1 Pressure Hi

ARP 2590A/D-10, Revision 000-02, Safety Injection Tank 1 Pressure Lo

AWO M2-04-01400, Safety Injection Tank Level Reduction Probably Leak at 2-SI-638 Identified

(CR-04-00877)

M2-EV-02-0029, Revision 00, HPSI Pump Availability During Surveillance Testing, dated

August 14, 2002

CR-02-07821, SP26048 Facility 2 HPSI OP and IST, Creates an Orange Risk Condition in MP2

Schedule and Needs to be Evaluated for Availability by Engineering

Service Water Brazed Joint Leakage

CR-04-02255, Entry into Unplanned LCO; Identified Leak from Service Water Piping in ESF;

The Leak is coming from Braze Joint Between 3SWP*V706 and 3SWP*V673

CR-04-02795, Poor Braze Penetration in Flange Joint Removed from MP3 Service Water

System

MP3 Maintenance Rule (a)(1) Evaluation for Service Water System, Revision 5

MP3 System Health Report - Service Water (3326), 2005 Quarter 1

MP3 Brazed Joint Inventory Table / Matrix Summary, dated September 01, 2005

MP3 SW Brazed Joint Table for 1 1/2 and Larger Diameter, dated March 21, 2005

Section 4OA5: Other Activities

CR-05-09287, Tracking CR for ISO-New England Procedure Revision

Attachment

A-12

LIST OF ACRONYMS

AC air conditioning

AFW auxiliary feedwater

AOP Abnormal Operating Procedure

CEA control element assembly

CFR Code of Federal Regulations

CR condition report

CVCS chemical and volume control system

DRP Division of Reactor Projects

DRS Division of Reactor Safety

ECCS emergency core cooling system

EDG emergency diesel generator

EOP Emergency Operating Procedure

ESF engineered safety feature

FSAR Final Safety Analysis Report

HELB high energy line break

HPSI high pressure safety injection

IMC Inspection Manual Chapter

LER licensee event report

LCO limiting condition of operation

MCC motor control center

MDAFWP motor-driven auxiliary feed water pump

MR Maintenance Rule

MSSV main steam safety valve

NCV non-cited violation

NRC Nuclear Regulatory Commission

OD Operability Determination

OWA operator work-around

PMT Post-Maintenance Test

RB reactor building

RBCCW reactor building closed cooling water

REMODCM Radiological Effluent Monitoring & Offsite Dose Calculation Manual

SDAFW steam-driven auxiliary feedwater

SDP significance determination process

SIH safety injection high

SIT safety injection tank

SORC Site Operations Review Committee

TI temporary instruction

TS technical specification

TDAFW turbine-driven auxiliary feedwater

Attachment