IR 05000255/2005004
ML051240380 | |
Person / Time | |
---|---|
Site: | Palisades |
Issue date: | 04/29/2005 |
From: | Lerch R NRC/RGN-III/DRP/RPB6 |
To: | Domonique Malone Nuclear Management Co |
References | |
IR-05-004 | |
Download: ML051240380 (38) | |
Text
ril 29, 2005
SUBJECT:
PALISADES NUCLEAR PLANT NRC INSPECTION REPORT 05000255/2005004
Dear Mr. Malone:
On March 31, 2005, the U. S. Nuclear Regulatory Commission (NRC) completed an inspection at your Palisades Nuclear Plant. The enclosed report documents the inspection findings which were discussed on March 31, 2005, with Mr. G. Hettel and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
Based on the results from this inspection period, one finding of very low safety significance (Green) was identified which involved a violation of NRC requirements. However, because the finding was of very low safety significance and because the issue has been entered into your corrective action program, the NRC is treating the violation as a Non-Cited Violation in accordance with Section VI.A.1 of the NRCs Enforcement Policy.
If you contest the subject or severity of a Non-Cited Violation, you should provide a response with a basis for your denial, within 30 days of the date of this inspection report, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission -
Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Palisades facility. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Robert M. Lerch, Acting Chief Branch 6 Division of Reactor Projects Docket No. 50-255 License No. DPR-20
Enclosure:
Inspection Report 05000255/2005004 w/Attachment: Supplemental Information
REGION III==
Docket No: 50-255 License No: DPR-20 Report No: 050000255/2005004 Licensee: Nuclear Management Company, LLC Facility: Palisades Nuclear Generating Plant Location: 27780 Blue Star Memorial Highway Covert, MI 49043-9530 Dates: January 1 through March 31, 2005 Inspectors: J. Lennartz, Senior Resident Inspector M. Garza, Resident Inspector C. Phillips, Senior Operations Engineer Approved by: Robert Lerch, Acting Chief Branch 6 Division of Reactor Projects Enclosure
SUMMARY OF FINDINGS
IR 05000255/2005004; 01/01/2005 - 03/31/2005; Palisades Nuclear Plant; Maintenance
Effectiveness.
This report covers a 3-month period of baseline resident inspections and announced inspections of licensed operator requalification training. The inspections were conducted by the resident inspectors and Region III inspectors. One Green finding with an associated Non-Cited Violation (NCV), was identified during this inspection period. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter 0609,
"Significance Determination Process (SDP)." Findings for which the SDP does not apply may be "Green" or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.
A. Inspector-Identified and Self-Revealed Findings
Cornerstone: Mitigating Systems
- Green.
The inspectors identified a finding of very low safety significance (Green)regarding the failure to implement corrective actions in a timely manner to identify why the component cooling water heat exchanger service water outlet valves failed to open in February 2003 and March 2003. Consequently, the cause was not identified and on January 16, 2005, CV-0826, "Component Cooling Water Heat Exchanger E-54B Service Water Outlet Valve," again failed to open when control room operators initially attempted to open the valve. The primary cause of this finding was related to the cross-cutting area of problem identification and resolution for failing to implement corrective actions.
This finding was more than minor because it was related to the equipment performance attribute of the mitigating systems cornerstone and the cornerstone objective to ensure the reliability and capability of systems that respond to initiating events to prevent undesirable consequences was adversely impacted. Specifically, the reliability and capability of CV-0826 to automatically open on a recirculation actuation signal and provide the required flow to the component cooling water heat exchangers was not ensured when CV-0826 failed to open on January 16, 2005.
The finding was of very low safety significance because the safety function was not lost.
A non-cited violation of 10 CFR 50 Appendix B, Criterion XVI, "Corrective Action," was identified. As an interim corrective action, both CV-0823 and CV-0826 are being cycled on an increased frequency to verify the valves will stroke open. Other planned corrective actions included installing a larger spring in the valve actuators to increase the opening force to overcome high frictional forces and to evaluate and implement appropriate modifications for the valves. (Section 1R12)
Licensee-Identified Violations
None.
REPORT DETAILS
A list of documents reviewed within each inspection area is included at the end of the report.
Summary of Plant Status
The plant operated at or near full power during the inspection period with the following two exceptions:
C On January 9, 2005, control room operators manually tripped the reactor because of a loss of condenser vacuum. After the cause for the loss of condenser vacuum was repaired, the reactor was taken critical on January 14, 2005. However, during startup activities for the main turbine, nonsafety-related turbine monitoring instrumentation indicated that a differential expansion existed between the turbine rotor and the turbine casing. Consequently, the main generator could not be synchronized to the electrical grid.
The reactor was maintained at approximately 1 percent power while licensee personnel investigated the cause for the differential expansion. The indications were subsequently determined to be erroneous because of degraded cables on the instrument probes that provided the signal for differential expansion. Following repairs to the turbine monitoring instrumentation, the main generator was synchronized to the electrical grid on January 19th. The plant was returned to full power on January 21st.
C On January 23, 2005, all four nonsafety-related moisture separator reheater steam supply valves unexpectedly closed. As a result, plant power was reduced to approximately 96 percent. A failed relay in the control circuitry for the valves was replaced and the plant was returned to full power on January 24th where it was maintained for the remainder of the inspection period.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness
1R04 Equipment Alignment
.1 Partial Walkdowns
a. Inspection Scope
The inspectors completed four equipment alignment inspection samples by performing partial walkdowns on the following risk-significant plant equipment:
- containment spray pumps P-54B and P-54C on January 25, 2005 while containment spray pump P-54A was out of service for planned maintenance;
- motor driven fire water pump P-9A and diesel driven fire pump P-9B on February 11, 2005, while diesel driven fire pump P-41 was out of service for emergent maintenance;
- component cooling water pump P-52A on February 23, 2005, while component cooling water pump P-52B was out of service for scheduled maintenance; and
- auxiliary feedwater pump P-8C on March 8, 2005, while auxiliary feedwater pump P-8B was out of service for scheduled maintenance.
During the walkdowns, the inspectors verified that power was available, that accessible equipment and components were appropriately aligned, and that no open work orders for known equipment deficiencies existed which would impact system availability.
The inspectors also reviewed selected condition reports related to equipment alignment problems and verified that identified problems were entered into the corrective action program with the appropriate significance characterization and that planned and completed corrective actions were appropriate and implemented as scheduled.
b. Findings
No findings of significance were identified.
.2 Complete Walkdown
a. Inspection Scope
The inspectors completed one semi-annual equipment alignment inspection sample by performing a complete walkdown of the emergency diesel generators. Utilizing piping and instrumentation diagrams and system checklists, the inspectors verified that accessible system components were correctly aligned. The inspectors also reviewed open maintenance work orders to verify that the equipments safety function was not adversely impacted by pending work.
The inspectors reviewed select condition reports associated with the emergency diesel generators to verify that identified problems were entered into the corrective action program with the appropriate significance characterization. The inspectors also verified that planned and completed corrective actions were appropriate.
b. Findings
No findings of significance were identified.
1R05 Fire Protection
.1 Fire Area Walkdowns
a. Inspection Scope
The inspectors completed eight fire protection inspection samples by touring the following areas in which a fire could affect safety-related equipment:
C fire area 1, control room complex C fire area 23D, critical function monitor computer trailer C fire area 8, emergency diesel generator fuel oil day tank room C fire area 9, intake structure C fire area 16, component cooling water pump room C fire area 22, turbine lube oil room C fire area 17, spent fuel pool room C fire are 24, auxiliary feedwater pump room The inspectors verified that transient combustibles and ignition sources were appropriately controlled, and that the installed fire protection equipment in the fire areas corresponded with the equipment which was referenced in the Updated Final Safety Analysis Report, Section 9.6, "Fire Protection." The inspectors also assessed the material condition of fire suppression systems, manual fire fighting equipment, smoke detection systems, fire barriers and emergency lighting units. For selected areas, the inspectors reviewed documentation for completed surveillances to verify that fire protection equipment and fire barriers were tested as required to ensure availability.
The inspectors reviewed select condition reports associated with fire protection to verify that identified problems were entered into the corrective action program with the appropriate significance characterization. The inspectors also verified that planned and completed corrective actions were appropriate.
b. Findings
No findings of significance were identified.
1R06 Flood Protection
a. Inspection Scope
The inspectors completed one inspection sample pertaining to flood protection for equipment designated in the Updated Final Safety Analysis Report to require protection from internal flooding due to failures of nonsafety-related systems. Specifically, the inspectors verified the adequacy of internal flood protection features for the emergency diesel generator 1-2 room.
The inspectors conducted walkdowns checking for applicability of the following attributes in the emergency diesel generator 1-2 room:
- holes or unsealed penetrations in floors, ceilings and walls
- common drain system and sumps, including floor drain piping
- sources of potential internal flooding that were not analyzed or were not adequately maintained The inspectors also reviewed selected condition reports related to flood protection problems and verified that identified problems were entered into the corrective action program with the appropriate significance characterization and that planned and completed corrective actions were appropriate and implemented as scheduled.
b. Findings
No findings of significance were identified.
1R11 Licensed Operator Requalification
.1 Quarterly Review
a. Inspection Scope
The inspectors completed one inspection sample pertaining to licensed operator requalification by observing licensed operators perform job performance measures during annual examinations on March 11, 2005. The inspectors assessed the operators ability to use plant procedures to perform the following tasks:
C reset variable high power trip setpoints from the thermal margin monitor screens C manually raise volume control tank level C shift 4160 V AC Bus 1A from station to startup power C locally start and load 1-1 diesel generator C open control rod drive clutch power supply breakers 42-1 and 42-2 The inspectors assessed the licensee evaluators' ability to administer the job performance measures and reviewed documentation to assess the evaluators ability to identify operator performance deficiencies.
b. Findings
No findings of significance were identified.
.2 Annual Operating Test Results
a. Inspection Scope
The inspectors reviewed the overall pass/fail results of Job Performance Measure (JPM)operating tests, simulator operating tests, and the biennial written examination (required to be given per 10 CFR 55.59(a)(2)) administered by the licensee from February 2 through April 1, 2005. The overall results were compared with the significance determination process in accordance with NRC Manual Chapter 0609I, "Operator Requalification Human Performance Significance Determination Process (SDP)."
This inspection counts as one sample.
b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness
a. Inspection Scope
The inspectors completed two inspection samples pertaining to maintenance effectiveness by reviewing maintenance rule implementation activities for the following system and components:
C radiation monitoring system C service water control valves CV-0823 and CV-0826 The inspectors reviewed the licensee's implementation of the maintenance rule requirements to verify that component and equipment failures were evaluated and appropriately dispositioned. The inspectors also verified that the selected systems and components were scoped into the maintenance rule and properly categorized as (a)(1)or (a)(2) in accordance with 10 CFR 50.65.
The inspectors reviewed the licensees maintenance rule performance indicators to verify that the equipment status had been appropriately categorized in accordance with the maintenance rule program; reviewed a sample of related condition reports written over the last 24 months to verify that the corrective actions for identified problems were appropriate; reviewed completed work orders and work order histories to determine if there was an adverse trend in equipment performance that could be attributed to inappropriate work practices; and, to determine if there were any common cause issues that had not been addressed. Additionally, the inspectors reviewed the licensees performance criteria to verify that the criteria adequately monitored equipment performance.
b. Findings
Introduction The inspectors identified a finding of very low safety significance (Green) regarding the failure to implement corrective actions in a timely manner to identify why the component cooling water heat exchanger service water outlet valves failed to open in February 2003 and March 2003. Consequently, the cause was not identified and on January 16, 2005, CV-0826, "Component Cooling Water Heat Exchanger E-54B Service Water Outlet Valve," again failed to open when control room operators initially attempted to open the valve Description Control valve CV-0826 was a normally closed valve and had a safety function to automatically open on a recirculation actuation signal. The valve actuator utilized air to close the valve and spring force to open the valve. On January 16, 2005, CV-0826 failed to open when control room operators initially attempted to open the valve using the control room handswitch. The operators were cycling the valve as part of a planned activity per plant procedures. The second attempt to open the valve from the control room was also unsuccessful. Before a third attempt, operators reduced air pressure to the valve actuator locally as directed by plant procedures and the valve was successfully opened using the control room handswitch.
The inspectors reviewed condition reports, maintenance rule evaluations, corrective actions, and work order history related to CV-0826 that had been generated since 2003.
The inspectors noted that CV-0826 had failed to fully open in February 2003 when control room operators initially attempted to open the valve. The control room operators successfully opened the valve on the second attempt. Because the valve did not fully open initially but successfully opened on the second attempt, the valve was characterized as operable but degraded. Licensee personnel concluded that this failure was most likely caused by increased amounts of sand in the service water system that was deposited near the valve disc after repeated cycling of dilution water pumps.
Subsequent to the failure of CV-0826 in February 2003, the opposite train control valve CV-0823, "Component Cooling Water Heat Exchanger E-54A Service Water Outlet Valve," failed to fully open in March 2003 during a scheduled refueling outage. Licensee personnel concluded that this failure was most likely caused by binding because of clearances in the coupling between the actuator and valve stem that allowed the actuator to position the valve disc into the seat further than desired. Corrective actions for CV-0823 were implemented during the outage which included adjustments to the actuator. The valve cycled satisfactorily during subsequent testing and was declared operable.
The inspectors concluded that the failures of CV-0823 and CV-0826 were appropriately characterized and dispositioned in accordance with the licensee's maintenance rule program. Also, several corrective actions were developed which were considered appropriate. For example, one corrective action, on an interim basis, was to increase the frequency at which CV-0826 was cycled while the valve was considered operable but degraded. Other corrective actions included developing preventive maintenance activities to monitor service water piping for sand buildup; revise appropriate plant procedures to direct actions for cycling CV-0823 and CV-0826 after dilution water pumps were started; and to collect diagnostic data when CV-0823 and CV-0826 were stroked for evaluation and trending.
In September 2004, an operability re-assessment for CV-0826 was completed prior to plant startup following the 2004 refueling outage which concluded the valve was fully operable and no longer operable but degraded. This reassessment took into account the corrective actions taken to date, improved performance of CV-0826 during increased cycling, and that little to no sand had been seen near CV-0823 or CV-0826 during ultrasonic testing of the service water piping.
On November 28, 2004, CV-0826 cycled satisfactorily during routine surveillance testing.
However, on January 16, 2005, CV-0826 again failed to open when the control room operators initially attempted to open the valve using the control room handswitch.
Licensee personnel concluded that this failure was caused by elevated frictional loads exceeding the capability of the valve actuator and preventing the valve from opening.
Licensee personnel also concluded that the elevated frictional forces were caused by probable seat deformation, high bearing loads and the presence of sand in the area between the disc and seat.
Thru a review of corrective action program documents, the inspectors noted that following the failures of CV-0823 and CV-0826 in 2003, other corrective actions were developed to overhaul the actuator and to disassemble and inspect the valve internals for CV-0823 during the 2004 refueling outage and CV-0826 during the 2006 refueling outage. Implementation of the corrective actions were scheduled for one valve at a time due to system configuration limitations and only during refueling outages.
Another corrective action was developed to factor any new information gained from the valve inspections into an apparent cause evaluation for past failures of CV-0823 and CV-0826 to document any additional actions needed to prevent future failures.
However, the corrective actions to rebuild the actuator and inspect the valve internals of CV-0823 were not implemented during the 2004 refueling outage because the work was removed from the outage scope. Therefore no new information was available for an apparent cause evaluation which impaired the ability of licensee personnel to definitively identify the cause for the valves failing to open. Consequently, additional actions needed to prevent future failures were not identified and CV-0826 again failed to open when initially attempted on January 16, 2005.
Analysis Failing to implement scheduled corrective actions impaired the ability to identify the cause for CV-0826 to not stroke fully open on demand and was considered a performance deficiency which warranted a significance evaluation. The inspectors determined that the finding was more than minor in accordance with Inspection Manual Chapter (IMC) 0612, Appendix B, "Issue Disposition Screening." The finding was related to the equipment performance attribute of the mitigating systems cornerstone and the cornerstone objective to ensure the reliability and capability of systems that respond to initiating events to prevent undesirable consequences was adversely impacted. Specifically, the reliability and capability of CV-0826 to automatically open on a recirculation actuation signal and provide the required flow to the component cooling water heat exchangers was not ensured when CV-0826 failed to open on January 16, 2005. However, in each instance that CV-0823 and CV-0826 initially failed to open, the operators were able to successfully open the valves on subsequent attempts without any corrective maintenance needed. Therefore, the inspectors concluded that a loss of safety function did not occur.
The finding was related to the cross-cutting area of problem identification and resolution for the failure to implement planned corrective actions. Corrective actions had been developed and scheduled to obtain additional information for identifying the cause of CV-0826 and CV-0823 failing to open in February 2003 and March 2003, respectively.
However, the corrective actions were not implemented during the 2004 refueling outage as scheduled. Consequently, the cause for the valves failing to open was not identified and corrected, and CV-0826 again failed to open on January 16, 2005.
Using IMC 0609, Appendix A, "SDP Phase 1 Screening Worksheet for IE [Initiating Events], MS [Mitigating Systems], and B [Barrier Integrity] Cornerstones," the inspectors determined that Mitigating Systems was the only cornerstone affected. Using the Mitigating Systems column on the Phase 1 SDP worksheet, the inspectors determined that the finding was:
- (1) not a design or qualification deficiency that had been confirmed to result in a loss of function per Generic Letter 91-18;
- (2) did not represent an actual loss of a safety function; and
- (3) did not screen as potentially risk significant due to a seismic, flooding, or severe weather event. Therefore, the finding screened as Green and was considered to be of very low safety significance.
Enforcement 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," requires, in part, that measures shall be established to assure that conditions adverse to quality, such as failures, are promptly identified and corrected. Contrary to this, the cause of CV-0826 failing to open on February 26, 2003, a condition adverse to quality, was not promptly identified and corrected. Consequently, on January 16, 2005, CV-0826 again failed to open when initially attempted by the control room operators.
However, because this violation was associated with a finding of very low safety significance and because the finding was entered into the licensees corrective action program, this violation is being treated as a Non-Cited Violation, consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000255/2005004-01).
This issue was entered into the licensees corrective action program as CAP046159.
As an interim corrective action, both CV-0823 and CV-0826 are being cycled on an increased frequency to verify the valves will stroke open. Other planned interim corrective actions included installing a larger spring in the valve actuators to increase the opening force to overcome high frictional forces. Long term corrective actions included evaluating and developing appropriate modifications for the valves.
1R13 Maintenance Risk Assessments and Emergent Work Evaluation
a. Inspection Scope
The inspectors completed five inspection samples regarding plant risk assessments for planned and emergent maintenance activities.
The inspectors reviewed Operators Risk Reports and documented safety assessments to verify that plant risk assessments were completed as required by 10 CFR 50.65(a)(4)prior to commencing maintenance activities; reviewed the Operations Log and daily maintenance schedules to verify that equipment necessary to minimize plant risk was operable or available as required during the planned and emergent maintenance activities; and conducted plant walkdowns to verify that equipment necessary to minimize risk was available for use. The inspection samples included the following activities:
C planned maintenance activities during the week of January 2, 2005, which included emergency diesel generator 1-1 testing and high pressure safety injection system testing.
C activities during the week of January 31, 2005, which included a planned maintenance outage on the emergency diesel generator 1-1, work on the containment spray pump P-54C breaker, and emergent maintenance on charging pump P-55A and diesel fire pump P-41.
C activities during the week of February 13, 2005, which included planned maintenance on service water traveling screen F-4B and auxiliary feedwater pump P-8C, planned surveillance testing on emergency diesel generator 1-2 and emergent maintenance on emergency diesel generator 1-2.
C planned preventive maintenance activities on March 8-9, 2005, for turbine driven auxiliary feedwater pump P-8B.
C planned preventive maintenance activities on March 15-16, 2005 for emergency diesel generator 1-2.
The inspectors also verified that condition reports related to emergent equipment problems were entered into the corrective action program with the appropriate significance characterization. Select condition reports related to risk management during maintenance activities were reviewed to verify that planned corrective actions were appropriate and had been implemented as scheduled.
b. Findings
No findings of significance were identified.
1R14 Operator Performance During Non-Routine Evolutions and Events
The inspectors completed two inspection samples regarding operator performance during the non-routine events described below.
.1 Loss of Main Condenser Vacuum
a. Inspection Scope
The inspectors reviewed control room logs and control board indications pertaining to a loss of main condenser vacuum that occurred on January 9, 2005. The inspectors verified that the control room operators implemented the actions in Off Normal Operating Procedure 14, "Loss of Main Condenser Vacuum," Off Normal Operating Procedure 26, "Rapid Power Reduction," and various annunciator response procedures as required.
The inspectors reviewed Condition Report CAP046023, "Loss of Main Condenser Vacuum," to verify that this problem was entered into the corrective action program with the appropriate significance characterization.
b. Findings
No findings of significance were identified.
.2 Moisture Separator Reheater Control Valves Unexpectedly Close
a. Inspection Scope
On January 23, 2005, all four nonsafety-related moisture separator reheater steam inlet valves unexpectedly closed and resulted in a slight loss of load with a reduction in reactor power from 100 percent to 96 percent. The inspectors reviewed control room logs, applicable data from the plant computer and plant procedures to verify that the control room operators implemented the actions in Off Normal Operating Procedure 1, "Loss of Load," as required in response to this non-routine evolution. The inspectors reviewed Condition Report CAP046288, "Spurious Closure of MSR (Moisture Separator Reheater) Supply Valves," to verify that this problem was entered into the corrective action program with the appropriate significance characterization. The inspectors reviewed condition reports for similar problems that had been previously entered into the corrective action program to verify that appropriate actions had been implemented.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations
a. Inspection Scope
The inspectors completed five inspection samples by reviewing documented operability assessments for the following risk-significant plant equipment:
- containment spray and low pressure safety injection systems
- reactor vessel level monitoring system
- reactor protective system
- component cooling water heat exchanger service water outlet valve CV-0826
- main steam safety valves The inspectors interviewed the cognizant engineers and reviewed the supporting documents to assess the adequacy of the operability assessments for the current plant mode or past operability as applicable. The inspectors also reviewed the applicable sections of the Technical Specifications, Updated Final Safety Analysis Report, and design basis documents to verify that the operability assessments were technically adequate and that the components remained available, such that no unrecognized increase in plant risk had occurred.
In addition, the inspectors verified that the condition reports generated for equipment operability issues were entered into the licensees corrective action program with the appropriate significance characterization.
b. Findings
No findings of significance were identified.
1R16 Operator Workarounds
a. Inspection Scope
The inspectors completed one inspection sample regarding operator workarounds by reviewing operator workaround OWA 05-01 "CV-0826 Component Cooling Water Heat Exchanger E-54B Service Water Outlet Valve." The inspectors verified that the functional capability of mitigating systems and the operators ability to implement off-normal and emergency operating procedures were not affected.
b. Findings
No findings of significance identified.
1R19 Post Maintenance Testing
a. Inspection Scope
The inspectors completed seven inspection samples pertaining to post maintenance testing by assessing testing activities that were conducted for the following maintenance activities:
C planned maintenance outage for emergency diesel generator 1-1 C plannned maintenance outage for auxiliary feedwater pump P-8C C emergent maintenance to remove, refurbish and reinstall the diesel driver for fire pump P-41 C planned maintenance on motor operated valve MO-3198, "Low Pressure Safety Injection Pump P-67A Inlet" C planned maintenance outage for auxiliary feedwater pump P-8B C planned maintenance outage for emergency diesel generator 1-2 C planned maintenance on service water pump P-7A breaker 52-204 The inspectors observed portions of the post maintenance testing and reviewed documentation to verify that the tests were performed as prescribed by the work orders and test procedures; that applicable testing prerequisites were met prior to the start of the tests; and, that the effect of testing on plant conditions was adequately addressed by the control room operators.
The inspectors reviewed documentation to verify that the test criteria and acceptance criteria were appropriate for the scope of work performed; reviewed test procedures to verify that the tests adequately verified system operability; and reviewed documented test data to verify that the data was complete, and that the equipment met the prescribed acceptance criteria.
Further, the inspectors reviewed condition reports to verify that post maintenance testing problems were entered into the corrective action program with the appropriate significance characterization. For select condition reports, the inspectors verified that the corrective actions were appropriate and implemented as scheduled.
b. Findings
No findings of significance were identified.
1R20 Refueling and Other Outage Activities
a. Inspection Scope
The inspectors completed one baseline inspection sample regarding other outage activities during a forced outage that occurred from January 9 through 19, 2005, after control room operators manually tripped the plant due to a loss of condenser vacuum.
The plant was maintained in Mode 3, "Hot Shutdown," while licensee personnel investigated the reason for the loss of vacuum. The inspectors monitored maintenance activities to verify that plant equipment necessary to minimize plant risk was maintained available and reviewed documentation to verify that appropriate cleanliness controls were implemented during maintenance inside containment. After necessary repairs were completed, the inspectors observed portions of reactor startup activities and main generator synchronization to the electrical grid to verify that the evolutions were completed in accordance with plant procedures.
The inspectors reviewed condition reports to verify that problems identified during the outage were entered into the corrective action program with the appropriate significance characterization. For select condition reports, the inspectors verified that appropriate corrective actions had been implemented.
b. Findings
No findings of significance were identified.
1R22 Surveillance Testing
a. Inspection Scope
The inspectors completed six inspection samples by assessing surveillance testing that was conducted on the following risk-significant plant equipment:
C containment isolation check valves C 2400 volt bus 1C undervoltage relays C emergency diesel generator 1-1 C battery charger number 4 C diesel fire pump P-41 C reactor coolant system The inspectors observed portions of the testing to verify that appropriate test procedures were utilized and reviewed documented test data to verify that test acceptance criteria were satisfied.
The inspectors reviewed applicable portions of Technical Specifications, the Updated Final Safety Analysis Report, and design basis documents to verify that the surveillance tests adequately demonstrated that the plant equipment could perform required safety functions.
Further, the inspectors reviewed selected condition reports regarding surveillance testing activities. The inspectors verified that the identified problems were entered into the licensees corrective action program with the appropriate significance characterization and that the planned and completed corrective actions were appropriate.
b. Findings
No findings of significance were identified.
1R23 Temporary Plant Modifications
.a Inspection Scope The inspectors completed three baseline inspection samples by reviewing the following temporary modifications:
C Temporary Modification 2005-001, "Swap Core Exit Thermocouple 27 With Core Exit Thermocouple 32" C Temporary Modification 2005-003, "Temporary Leak Repair on Atmospheric Dump Valve Instrument Air Supply Header" C Temporary Modification 2005-005, "Disabling the Automatic Re-closure of Pressurizer Heater Circuit Breaker 152-211" The inspectors reviewed the design documents, 10 CFR 50.59 safety screening, Updated Final Safety Analysis Report, and applicable technical specifications and their bases to verify that the temporary modifications did not affect the operability of the related systems and other interfacing systems. The inspectors reviewed documentation and conducted plant walkdowns of accessible equipment using applicable procedures and plant drawings to verify that the modifications were implemented as designed. Post modification testing results were reviewed to verify that the systems functioned as intended after the modifications were implemented.
b. Findings
No findings of significance were identified.
1EP6 Emergency Preparedness Drill Evaluation
The inspectors completed two baseline inspection samples by evaluating the emergency preparedness drills described below.
.1 Tabletop Drill In Technical Support Center
a. Inspection Scope
The inspectors observed a training drill on January 26, 2005, in the Technical Support Center in which the site emergency director was required to implement the emergency plan in response to simulated plant conditions. Emergency Preparedness personnel had pre-designated that the opportunities for the site emergency director to classify the event and make protective action recommendations would be evaluated and included in the performance indicator data regarding drill and exercise performance.
The inspectors verified that the site emergency director classified the emergency condition and completed protective action recommendations in an accurate and timely manner as required by the emergency plan implementing procedures. The inspectors reviewed documentation to verify that the performance indicator data regarding drill and exercise performance was accurately accounted for.
b. Findings
No findings of significance were identified.
.2 1st Quarter 2005 Emergency Planning Drill
a. Inspection Scope
The inspectors observed emergency response personnel in the Technical Support Center and the Emergency Offsite Facility during an emergency planning drill conducted on February 22, 2005. Emergency Preparedness personnel had pre-designated that the opportunities to classify the event and make protective action recommendations would be evaluated and included in the performance indicator data regarding drill and exercise performance.
The inspectors verified that the emergency classifications, notifications to offsite agencies, and the development of protective action recommendations were completed in an accurate and timely manner as required by the emergency plan implementing procedures. The inspectors also verified that the drill was conducted in accordance with the prescribed sequence of events and that the drill objectives were met.
The inspectors observed the post-drill critique in the Technical Support Center and the Emergency Offsite Facility to verify that emergency response personnel and drill evaluators adequately self-identified performance problems. The inspectors reviewed the post-drill critique report to verify that the data regarding the indicator for drill and exercise performance was accurate. Condition reports generated for identified drill performance problems were reviewed to verify that the problems were entered into the corrective action program with the appropriate significance characterization.
b. Findings
No findings of significance were identified.
OTHER ACTIVITIES (OA)
4OA2 Identification and Resolution of Problems
.1 Routine Review of Identification and Resolution of Problems
a. Inspection Scope
As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that condition reports were being generated and entered into the corrective action program with the appropriate significance characterization. For select condition reports, the inspectors also verified that identified corrective actions were appropriate and had been implemented or were scheduled to be implemented in a timely manner commensurate with the significance of the identified problem.
b. Findings
No findings of significance were identified.
.2 Annual Sample for Follow-up Inspection
a. Inspection Scope
The inspectors completed two inspection samples regarding annual reviews of problem identification and resolution evaluations by reviewing the following cause evaluations:
- Root Cause Evaluation RCE000367, "Inadvertent Safety Injection Actuation During Surveillance Test RO-12"
- Apparent Cause Evaluation ACE003392, "Component Cooling Water P-52A Secured Due to Failure of the Outboard Motor Bearing" The inspectors verified that:
- (1) the problems were accurately identified;
- (2) the root cause, apparent cause, and contributing causes were adequately justified;
- (3) extent of condition and generic implications were appropriately addressed;
- (4) previous occurrences were considered; and
- (5) corrective actions were appropriately focused to address the problem and implemented commensurate with the safety significance of the issue.
b. Findings
No findings of significance were identified.
4OA3 Event Follow-up
The inspectors completed four inspection samples related to event follow-up as described below.
.1 Manual Reactor Trip For Loss of Condenser Vacuum
a. Inspection Scope
The inspectors responded to the control room on January 9, 2005, after being notified that the control room operators manually tripped the reactor because of lowering main condenser vacuum. The inspectors walked down the control panels to verify that plant parameters were stable and as expected, and to verify that safety-related equipment was operating as expected. The inspectors reviewed control room logs, plant procedures, and the event notification that was provided to the NRC, and observed post-trip response actions in the control room. The inspectors verified that control room operators implemented the required actions in emergency operating procedures while responding to and recovering from the plant trip, and that the plant trip was communicated to the NRC in a timely and accurate manner. The inspectors reviewed Condition Report CAP046023, "Loss of Main Condenser Vacuum," to verify that this problem was entered into the corrective action program with the appropriate significance characterization.
b. Findings
No findings of significance were identified.
.2 (Closed) Licensee Event Report (LER) 2004-003: Main Steam Safety Valves Exceed
Lift Setpoint Acceptance Band During main steam safety valve setpoint testing, 11 out of 24 valves had as-found lift pressures that were above the acceptance band. Technical Specification Limiting Condition of Operation 3.7.1 required a minimum of 23 out of 24 valves to be operable in Modes 1, 2 and 3. Since 11 of the 24 valves were likely inoperable during the last operating cycle, this was reported in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by Technical Specifications.
The inspectors reviewed the LER to verify that the event was accurately described, to determine if any violations of NRC requirements occurred and to assess the appropriateness of corrective actions. A cause evaluation, significance evaluation and long-term corrective actions were incomplete when this LER was submitted and were to be provided in a supplemental report. Therefore, the inspectors assessed the significance of any potential violations of NRC requirements and appropriateness of long term corrective actions after the supplemental report was issued which is documented in Section 4OA3.3 of this report.
This issue was entered into the licensee's corrective action program as Condition Report CAP045638, "RV-0720 AS -Found Test Exceeds Acceptance Range of RM-29." For immediate corrective actions, all 11 safety valves that failed to lift within the acceptance criteria were adjusted, as necessary, and retested satisfactorily which restored compliance with Technical Specifications.
The inspectors identified one inaccurate statement in the LER section describing the cause of the event. The inspectors noted that this same error was also contained in the supplemental report referenced in Section 4OA3.3 of this report. Specifically, the report indicated that during the second lift attempt, all but two main steam safety valves lifted within the as-found acceptance criterion, and for those two they lifted below the acceptance band. However, the data in Table 1 attached to the LER did not support that statement. The data in Table 1 was verified to be correct and therefore, only one main steam safety valve lifted below the as-found acceptance band on the second lift attempt instead of two as stated. This inaccurate statement did not change the significance of the event and therefore was considered to be an administrative error of minor significance. This LER is closed.
.3 (Closed) LER 2004-003-01: Main Steam Safety Valves Exceed Lift Setpoint Acceptance
Band This supplemental report provided updated information pertaining to the cause evaluation, significance evaluation and long-term corrective actions for 11 out of 24 main steam safety valves which lifted above the acceptance band during setpoint testing.
Technical Specification Limiting Condition of Operation 3.7.1 required a minimum of 23 out of 24 valves to be operable in Modes 1, 2 and 3. Since 11 of the 24 valves were likely inoperable during the last operating cycle, this event was initially reported in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by Technical Specifications. The inspectors reviewed this supplemental report to determine if any violations of NRC requirements occurred and to assess long term corrective actions.
Licensee personnel concluded that a combination of disc to seat sticking, and valve spindle binding/bonding at the guide bearing caused the high lift setpoints. Although 11 out of 24 valves were likely inoperable during the previous operating cycle, a condition prohibited by Technical Specifications, a subsequent evaluation concluded that during events which credited operation of the main steam safety valves neither the acceptance criteria nor plant design limits would have been challenged with this as-found condition.
Consequently, this event had little to no potential to impact plant safety. Also, there were no actual safety consequences and the event had no impact on the regulatory process and did not involve willfulness. Therefore, this event constituted a violation of Technical Specifications which was determined to be of minor significance in accordance with Section IV of the NRC Enforcement Policy.
As a long-term corrective action, licensee personnel developed a maintenance and testing plan to test the main steam safety valves on a more frequent basis which was considered appropriate. This LER is closed.
.4 (Closed) LER 2005-001: Reactor Protection System and Auxiliary Feedwater System
Actuation On January 9, 2005, a rapid plant down power was commenced from full power due to an unexpected lowering of condenser vacuum. The reactor was subsequently manually tripped from 75 percent power. Following the trip, the auxiliary feedwater system started automatically to maintain steam generator water level. All safety systems functioned as expected during the plant trip and the plant was stabilized in Mode 3. A nonsafety-related low pressure turbine casing drain line, which was routed through the main condenser, failed and allowed air in-leakage into the main condenser which caused the lowering vacuum. Corrective actions were implemented to permanently plug the drain line. Operator response to this event was assessed and documented in Section 4OA3.1 of this report and no findings of significance were identified. This event did not constitute a violation of NRC requirements. This problem was entered into the licensee's corrective action program as Condition Report CAP046023, "Loss of Main Condenser Vacuum." This LER is closed.
4OA4 Cross Cutting Aspects of Findings
.1 A finding described in Section 1R12 of this report had, as a primary cause, a problem
identification and resolution deficiency. Licensee personnel failed to implement planned corrective actions as initially scheduled which impaired the ability to identify the cause of service water control valves CV-0823 and CV-0826 failing to open. Consequently, the cause was not corrected and CV-0826 again failed to open on January 16, 2005.
4OA6 Meetings
.1 Exit Meeting
The inspectors presented the inspection results to Mr. G. Hettel and other members of licensee management on March 31, 2005. Licensee personnel acknowledged the findings presented. The inspectors asked licensee personnel whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.
.2 Interim Exit Meeting
Interim exit was conducted for:
- Licensed Operator Requalification 71111.11B with Mr. J. Walker, Licensed Operator Requalification Training Supervisor, on April 11, 2005, via telephone.
ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee
- D. Malone, Site Vice President
- P. Harden, Site Director
- T. Blake, Emergency Preparedness Supervisor
- M. Carlson, Engineering Director
- G. Hettel, Plant Manager
- L. Lahti, Licensing Manager
- D. Malone, Regulatory Affairs
- K. Smith, Operations Manager
- J. Walker, Licensed Operator Requalification Training Supervisor
- K. Yeager, Assistant Operations Manager
Nuclear Regulatory Commission
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
2005004-01 NCV Failure to implement corrective actions which impaired the ability to identify the cause of CV-0823 and CV-0826 failing to open (Section 1R12)
Closed
2005004-01 NCV Failure to implement corrective actions which impaired the ability to identify the cause of CV-0823 and CV-0826 failing to open (Section 1R12)
- 05000255/04-003 LER Main Steam Safety Valves Exceeded Lift Setpoint Acceptance Band (Section 4OA3.2)
- 05000255/04-003-01 LER Main Steam Safety Valves Exceeded Lift Setpoint Acceptance Band (Section 4OA3.3)
- 05000255/05-001 LER Reactor Protection System and Auxiliary Feedwater System Actuation (Section 4OA3.4)
Discussed
None Attachment