ML021160683

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IR 05000266/2002-005; 05000301/2002-005, on 02/20-03/31/2002, Nuclear Management Company, LLC, Point Beach Nuclear Plant, Units 1 & 2. Operability Evaluations
ML021160683
Person / Time
Site: Point Beach  NextEra Energy icon.png
Issue date: 04/26/2002
From: Lanksbury R
NRC/RGN-III/DRP/RPB5
To: Warner M
Nuclear Management Co
References
IR-02-005
Download: ML021160683 (33)


See also: IR 05000266/2002005

Text

April 26, 2002

Mr. M. Warner

Site Vice President

Kewaunee and Point Beach Nuclear Plants

Nuclear Management Company, LLC

6610 Nuclear Road

Two Rivers, WI 54241

SUBJECT: POINT BEACH NUCLEAR PLANT

NRC INSPECTION REPORT 50-266/02-05; 50-301/02-05

Dear Mr. Warner:

On March 31, 2002, the NRC completed an inspection at your Point Beach Nuclear Plant. The

enclosed report documents the inspection findings which were discussed on April 5, 2002, with

you and members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel. Specifically, this inspection was a routine review of plant activities by resident and

regional inspectors.

Based on the results of this inspection, the inspectors identified one finding for which the safety

significance was still to be determined. This issue pertained to the self-revealing failure of the

Unit 2 'B' train safety injection pump, 2P-15B, due to gas binding on February 20, 2002. The

issue was determined to be of at least very low safety significance (Green) since one train of

the Unit 2 safety injection system was rendered inoperable.

M. Warner -2-

In accordance with 10 CFR 2.790 of the NRCs "Rules of Practice," a copy of this letter

and its enclosure will be available electronically for public inspection in the NRC Public

Document Room or from the Publicly Available Records System (PARS) component of NRCs

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Roger D. Lanksbury, Chief

Branch 5

Division of Reactor Projects

Docket Nos. 50-266; 50-301

License Nos. DPR-24; DPR-27

Enclosure: Inspection Report 50-266/02-05; 50-301/02-05

cc w/encl: R. Grigg, President and Chief

Operating Officer, WEPCo

R. Anderson, Executive Vice President

and Chief Nuclear Officer

T. Webb, Licensing Manager

D. Weaver, Nuclear Asset Manager

T. Taylor, Plant Manager

A. Cayia, Site Director

J. ONeill, Jr., Shaw, Pittman,

Potts & Trowbridge

K. Duveneck, Town Chairman

Town of Two Creeks

D. Graham, Director

Bureau of Field Operations

A. Bie, Chairperson, Wisconsin

Public Service Commission

S. Jenkins, Electric Division

Wisconsin Public Service Commission

State Liaison Officer

To receive a copy of this document, indicate in the box:"C" = Copy without enclosure "E"= Copy with enclosure"N"= No copy

OFFICE RIII RIII N

NAME MKunowski/trn RLanksbury

DATE 04/26/02 04/26/02

OFFICIAL RECORD COPY

M. Warner -3-

ADAMS Distribution:

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BAW

RidsNrrDipmIipb

GEG

HBC

PGK1

C. Ariano (hard copy)

DRPIII

DRSIII

PLB1

JRK1

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos: 50-266; 50-301

License Nos: DPR-24; DPR-27

Report No: 50-266/02-05; 50-301/02-05

Licensee: Nuclear Management Company, LLC

Facility: Point Beach Nuclear Plant, Units 1 & 2

Location: 6610 Nuclear Road

Two Rivers, WI 54241

Dates: February 20 through March 31, 2002

Inspectors: P. Krohn, Senior Resident Inspector, Point Beach

J. Lara, Senior Resident Inspector, Kewaunee

Z. Dunham, Resident Inspector, Kewaunee

D. Chyu, Reactor Engineer

B. Winters, Reactor Inspector

Approved by: Roger D. Lanksbury, Chief

Branch 5

Division of Reactor Projects

SUMMARY OF FINDINGS

IR 05000266-02-05; 05000301-02-05, on 02/20-03/31/2002, Nuclear Management

Company, LLC, Point Beach Nuclear Plant, Units 1 & 2. Operability Evaluations.

This report covers a 6-week routine resident inspection. The inspection was conducted by

resident and regional inspectors. The inspection identified one finding of at least very low

safety significance (Green) that, pending further regulatory review, was considered an

Unresolved Item. The significance of most findings is indicated by their color (Green, White,

Yellow, Red) using Inspection Manual Chapter 0609, Significance Determination Process.

Findings for which the Significance Determination Process does not apply are indicated by

No Color or by the severity level of the applicable violation. The NRCs program for

overseeing the safe operation of commercial nuclear power reactors is described at its Reactor

Oversight Process website at http://www.nrc.gov/NRR/OVERSIGHT/ASSESS/index.html.

A. Inspector-Identified Findings

Cornerstone: Mitigating Systems

  • To Be Determined (TBD). Unit 2. On February 20, 2002, the 2P-15B safety

injection pump failed, during monthly preventative maintenance bearing

lubrication activities, due to gas binding caused by back-leakage of nitrogen-

saturated water from a reactor coolant system safety injection accumulator.

Despite multiple opportunities to have identified the effects of the leaking

accumulator, the licensee's organization did not properly respond to adverse

accumulator leakage trends or effectively use industry operating experience to

prevent failure of the safety injection pump. This issue was considered an

Unresolved Item pending further regulatory review of the risk and problem

identification and resolution aspects of the safety injection pump failure.

This issue was determined to have a credible impact on safety and be of at least

very low safety significance (Green) since one train of the Unit 2 safety injection

system was rendered inoperable. (Sections 1R15.1 and 4OA2)

B. Licensee-Identified Findings

A licensee-identified violation of very low significance was reviewed by the inspectors.

Corrective actions taken or planned by the licensee appeared reasonable. The violation

is listed in Section 4OA7 of this report.

2

Report Details

Summary of Plant Status

Unit 1 began the inspection period at full power and remained there until March 23, 2002, when

power was reduced to 30 percent to lower the worker radiation dose during restoration of a

reactor coolant system (RCS) wide-range pressure transmitter, turbine stop and governor valve

testing, condenser and crossover steam dump valve testing, atmospheric steam dump testing,

and repair of an oil leak on the 1P-28A main feed pump. Unit 1 was returned to full power

operation on the morning of March 24. Unit 1 remained at full power until March 30, when an

emergency operating facility computer networking problem caused the plant process computer

system to be declared unreliable. Reactor power was reduced to 97 percent during

troubleshooting efforts. Unit 1 was returned to full power operation on March 31 and remained

there through the end of the inspection period.

Unit 2 began the inspection period at full power and remained there until a Technical

Specification (TS) required forced-shutdown due to failure of the 2P-15B safety injection (SI)

pump on February 22, 2002. Following SI pump repairs and testing, Unit 2 was made critical

on February 25, and returned to full power operations on February 26. Unit 2 power was

reduced to 97 percent on March 19, due to a plant process computer failure that occurred while

loading software upgrades. Unit 2 was returned to full power operation later the same day

following correction of the software problems. Unit 2 remained at full power until March 30,

when an emergency operating facility computer networking problem caused the plant process

computer system to be declared unreliable. Reactor power was reduced to 97 percent during

troubleshooting efforts. Unit 2 was returned to full power operation on March 31 and remained

there through the end of the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events and Mitigating Systems

1R04 Equipment Alignment (71111.04)

.1 125-Volt Direct Current (VDC) Partial System Walkdown

a. Inspection Scope

The inspectors performed a partial system walkdown of the Units 1 and 2 125-VDC

distribution system to verify proper system configuration. The inspectors used licensee

checklists (CLs), weekly TS tests, and operating procedures during the walkdowns to

verify that the systems were properly configured for full power operations. The CLs and

TS tests were compared against design basis requirements to verify that the documents

aligned the 125-VDC system in accordance with design basis assumptions. The

inspectors also performed walkdowns in the control room to verify appropriate switch

positions and valve configurations.

The inspectors reviewed action request (AR) 2652, PC-43 Part 2, which was initiated

as a result of this inspection activity and discussed seven breakers, including the power

3

supply to a solenoid valve associated with the Unit 2 turbine-driven auxiliary feedwater

(TDAFW) pump recirculation valve, that were not included in the monthly, safety-related,

continuous-use CL. The inspectors also reviewed the document feedback form for

PC-43 Part 2, Revision 32, to verify that the missed breakers had been added to the

next revision of the CL. Finally, the inspectors evaluated other elements, such as

material condition, housekeeping, and component labeling.

b. Findings

No findings of significance were identified.

.2 Unit 2 TDAFW System Partial Walkdown Following Mini-Recirculation Valve

Accumulator Modification

a. Inspection Scope

The inspectors performed a partial system walkdown of the Unit 2 TDAFW pump

system to verify proper system configuration following modifications to provide a

nitrogen backup accumulator to the mini-recirculation valve, 2AF-4002. The inspectors

used licensee CL 13E, Part 1, Auxiliary Feedwater Valve Lineup Turbine Driven, during

the walkdowns to verify that the system was properly configured for full power

operations. The CL and safety evaluation used to install the nitrogen backup

accumulator were compared against design requirements to verify that the accumulator

had been installed in accordance with design basis assumptions. The inspectors

performed walkdowns in the control room, primary auxiliary building, Unit 2 facade,

cable spreading room, turbine building, and the auxiliary feedwater pump room to verify

appropriate switch and valve positions. The inspectors also reviewed the completed

copy of CL 13E, Part 1, to verify that auxiliary operators had used independent

verification and self-checking human performance techniques to identify typographical

errors and incomplete position designations for some of the newly installed backup

nitrogen accumulator valves associated with the Unit 2 TDAFW pump system. Finally,

the inspectors evaluated other elements, such as material condition, housekeeping, and

component labeling.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

a. Inspection Scope

The inspectors walked down the following areas to assess the overall readiness of fire

protection equipment and barriers:

  • Fire Zone 310, Air Compressor Room
  • Fire Zone 246, Electrical Equipment Room - Unit 2
  • Fire Area A26, Fire Zone 307, Battery Room D-05

4

Emphasis was placed on the control of transient combustibles and ignition sources, the

material condition of fire protection equipment, and the material condition and

operational status of fire barriers used to prevent fire damage or propagation. Area

conditions/configurations were evaluated based on information provided in the

licensees Fire Hazards Analysis Report, August 2001.

The inspectors toured the three fire zones to verify that fire hoses, sprinklers, and

portable fire extinguishers were installed at their designated locations, were in

satisfactory physical condition, and were unobstructed and to verify the physical location

and condition of fire detection devices. Additionally, passive features such as fire doors,

fire dampers, and mechanical and electrical penetration seals were inspected to verify

that they were located per Fire Hazards Analysis Report requirements and were in good

physical condition.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification (71111.11)

.1 Resident Inspector Quarterly Review: Shutdown Loss-of-Coolant Accident (LOCA)

a. Inspection Scope

On March 19, 2002, the resident inspectors observed licensed operator training

involving a LOCA while shutdown. The scenario was applied to both Units. The

inspectors evaluated crew performance for clarity and formality of communication; the

ability to take timely action in the safe direction; the prioritizing, interpreting, and

verifying of alarms; the correct use and implementation of procedures, including alarm

response procedures; timely control board operation and manipulation, including

high-risk operator actions; and group dynamics.

b. Findings

No findings of significance were identified.

1R12 Maintenance Rule Implementation (71111.12)

a. Inspection Scope

The inspectors reviewed the implementation of the maintenance rule to verify that

component and equipment failures were identified, entered, and scoped within the

maintenance rule and that select structures, systems and components were properly

categorized and classified as (a)(1) or (a)(2) in accordance with 10 CFR 50.65. The

inspectors reviewed station logs, maintenance work orders (WOs), condition reports

(CRs), ARs, (a)(1) corrective action plans, selected surveillance test procedures, and a

sample of CRs to verify that the licensee was identifying issues related to the

maintenance rule at an appropriate threshold and that corrective actions were

appropriate. Additionally, the inspectors reviewed the licensees performance criteria to

5

verify that the criteria adequately monitored equipment performance and to verify that

licensee changes to performance criteria were reflected in the licensees probabilistic

risk assessment. Specific components and systems reviewed were:

  • 480-Volt Alternating Current Electrical System
  • Instrument Air

b. Findings

No findings of significance were identified.

1R14 Personnel Performance During Non-Routine Plant Evolutions (71111.14)

.1 Unit 2 Forced Shutdown Due to 'B' SI Pump Failure

a. Inspection Scope

The inspectors observed control room activities associated with a Unit 2 forced

shutdown on February 22, 2002, following failure of the 2P-15B SI pump due to gas

binding on February 20, 2002. Since repair of the pump was expected to exceed the

72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> allowed in TS Action Condition Requirement 3.5.2, the licensee commenced a

normal shutdown and progression to cold shutdown, as reported in Event

Notification 38718. The inspectors assessed the adequacy of operations activities

during the reduction of electrical load, reactor shutdown, plant cooldown, and

stabilization of RCS temperature and pressure above the residual heat removal (RHR)

system initiation point. Additionally, the inspectors reviewed maintenance operations for

implementation of risk management, conformance to approved site procedures, and

compliance with TS requirements. The inspectors reviewed 5 ARs written as a result of

the forced shutdown, including AR 2284, Unit 2 Shutdown to Mode 4 Almost Causes a

UE [Unusual Event] Entry; AR 2289, AOP [Abnormal Operating Procedure] 8A, High

Coolant Activity, Is Unclear On When To Restore Normal PAB [Primary Auxiliary

Building] Access; and AR 2323, U2 N32 Source Range Detector Failure With Less

Than One Cycle of Operation.

b. Findings

No findings of significance were identified.

.2 Personnel Performance During Propane Leak

a. Inspection Scope

On March 4, 2002, the inspectors observed control room crew actions during a propane

leak from a 500-gallon storage tank adjacent to a well water pumphouse. The propane

tank was located outside of the protected area. The propane leak was considered a

Toxic/Flammable Gas Intrusion and classified as an Unusual Event by the licensee.

Offsite fire department assistance was requested and obtained from the Town of Two

Creeks volunteer fire department. The propane leak was reported to the NRC under

Event Notification Number 38749.

6

The inspectors monitored licensee communications and actions to ascertain whether

appropriate personnel evacuations were considered; to determine the possible ignition

impact of the propane leak on adjacent fuel oil storage tanks and switchyard electrical

distribution lines; to monitor propane sampling results to determine if explosive

atmospheres existed in any portions of the nearby turbine building or vital equipment

areas; to monitor licensee actions in determining whether personnel evacuations from

selected site locations were required; and to monitor contractor and offsite fire

department efforts to stop the propane leak. The inspectors considered wind velocities,

ambient temperatures, projected wind shifts, and the rate of the propane tank inventory

loss to determine the potential impact of the leak on site equipment and operations.

The inspectors also monitored initial manning of the technical support center to

determine licensee preparation for potentially worsening conditions. Finally, the

inspectors reviewed AR 2448, Unusual Event Declared on March 4, 2002: Lack of

Plant Guidance, which discussed the lack of orders to terminate smoking or other spark

producing activities during the initial stages of the propane leak.

b Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

.1 2P-15B SI Pump Failure Due to Gas Binding During Monthly Lubrication Run

a. Inspection Scope

The inspectors reviewed a self-revealing failure of the 2P-15B Unit 2 SI pump on

February 20, 2002. During the subsequent repair and replacement activities, the

inspectors conducted reviews to verify compliance with TS action condition statements;

observed pump disassembly and reassembly; inspected failed parts; reviewed post-

maintenance testing activities; and reviewed Final Safety Analysis Report (FSAR)

design requirements. The inspectors also reviewed Operability Determination

(OBD) 000011, Gas Binding of SI Pumps, to verify that the licensee had considered

the potential effects of gas binding on:

  • Unacceptable water hammers due to the rapid refilling of voided SI injection lines

upon pump start

  • Gas migration to other piping that may have rendered adjacent emergency core

cooling system (ECCS) equipment sharing common suction piping inoperable

  • Accident analyses due to a delay in injecting water into the reactor core as a

result of having voided volumes in the SI pump discharge lines

  • Various leaking (or failed open) valves in the system
  • Flow and pressure instrument sensing lines
  • Pressure-locking SI system valves during pressure transients
  • Load amplification due to the constructive combination of reflected shock waves

in partially voided SI injection lines.

The inspectors evaluated the OBD to verify that the venting locations, frequency, and

instructions given to auxiliary operators for the conduct of venting were conservative and

7

maintained SI pump operability. The inspectors reviewed SI and residual heat removal

(RHR) pump suction and discharge piping isometric drawings to determine available

venting points, the creation and effect of loop-seals for unventable portions of the

injection line, and the extent to which voided gas volumes could have migrated back

towards other ECCS pumps. The inspectors interviewed selected engineering

personnel and reviewed pump internal drawings to determine the effects of varying

pump casing gas volumes on SI pump operability. The inspectors reviewed the impact

of 2SI-845E, Unit 2 2P-15B SI Pump To Reactor Coolant Loop 'A' Cold Leg SI Check

Valve, back-leakage on TS 3.4.14 RCS pressure insolation valve leak rate

requirements. The inspectors also reviewed the licensee's troubleshooting plan to

identify the leakage path from the Unit 2 'A' SI accumulator, 2T-34A, back to the 2P-15B

SI pump casing and future check valve repair plans.

The inspectors reviewed Operating Instruction (OI) 163, SI, RHR, and CS [Containment

Spray] Pump Runs, Revision 1, to determine whether monthly SI pump runs for

preventative maintenance bearing lubrication activities constituted preconditioning for

TS required quarterly surveillance tests. The inspectors applied the results of

OBD 000011 to both Units 1 and 2 to verify that the licensee had considered the full

effects of accumulator back leakage on all ECCS equipment.

The inspectors interviewed selected engineering personnel and correlated Unit 2 A SI

accumulator level and pressure history, 2P-15B SI pump injection line volumes, and

nitrogen solubility data to determine when the 2P-15B SI pump had become inoperable.

Finally, the inspectors considered previous licensee operating experience (OE) and

corrective action program opportunities to have prevented failure of the 2P-15B SI

pump.

b. Findings

Self-Revealing Condition

On February 20, 2002, at 1:00 a.m., the 2P-15B SI pump was started in accordance

with OI-163 as part of a monthly preventative maintenance bearing lubrication activity.

The control room operators noted that when the pump was started, motor current

increased normally, but then decayed to less than 10 amps. The normal SI pump

running current was 30 amps. Additionally, the pump developed no discharge pressure.

The auxiliary operator stationed locally in the vicinity of the SI pump noted a loud noise

near the end of the pump coastdown, observed excessive seal leakage, and reported

the presence of an acrid smell to the control room. The Duty Shift Superintendent

arrived in the pump area shortly thereafter, observed the excessive seal leakage, and

perceived the acrid smell. Through follow-up discussion and observation it was

concluded that the acrid smell was emanating from the inboard pump seal area. The

Duty Shift Superintendent (the lead Senior Reactor Operator on-shift) directed the

isolation of the pump to secure the excessive seal leakage. The 2P-15B SI pump was

declared inoperable and TS Action Condition 3.5.2.A.1 entered at 1:00 a.m. on

February 20, 2002. Technical Specification Action Condition 3.5.2.A.1 required an

inoperable ECCS train be restored to operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or the affected

Unit be placed in Mode 3 (Hot Standby) within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and Mode 4 (Hot

Shutdown) within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

8

Subsequent licensee inspection of the pump revealed damage to the rotating element,

the coupling and shaft keys between the pump and the motor, the pump internal

wearing rings, and other components. The licensee concluded that the cause of the

equipment damage was pump gas binding as the result of back-leakage of nitrogen-

saturated water from the SI A accumulator through at least two check valves,

2SI-845E, Unit 2 2P-15B SI Pump To Reactor Coolant Loop 'A' Cold Leg SI Check

Valve, and 2SI-889B, Unit 2 2P-15B SI Pump Discharge Check Valve, to the

discharge side of the 2P-15B pump. When the pressure of the nitrogen-saturated water

was reduced from the accumulator pressure (750 pounds per square inch gauge) to the

SI pump suction pressure (~30 pounds per square inch gauge), the nitrogen came out

of solution, causing the 2P-15B gas binding.

The licensee proceeded with the repair of 2P-15B with the expectation that the pump

would be repaired, tested, and returned to service prior to the expiration of 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> TS

Action Statement 3.5.2.A.1. At approximately 2:00 p.m. on February 22, 2002, the

licensee determined that pump repairs and testing could not be completed before the

expiration of the TS action statement. Accordingly, shutdown of Unit 2 began at

2:48 p.m. Mode 3 was reached at 7:26 p.m., and Mode 4 at 1:38 a.m. on

February 23, 2002. Operator performance during the shutdown was reviewed in

Section 1R14.1 of this report. During the time that the Unit 2 'B' ECCS train was

inoperable, the A' ECCS train remained in standby service and was capable of

performing the intended safety function.

Operability of 2P-15B SI and Other ECCS Pumps

The inspectors reviewed and found acceptable, the licensee's OBD conclusion that

venting the SI lines at least every 5 days was sufficient to ensure continued operability

of the Units 1 and 2 SI pumps. The frequency was based on observed accumulator

leakage history and would increase proportionately if accumulator leakage rates

increased. The inspectors also concluded that the Units 1 and 2 'A' train SI pumps had

remained operable since these pumps had been run frequently to refill SI accumulators

and had effectively swept any nitrogen-saturated water or gas voids back into the

accumulators each time the pumps were run. The Unit 1 'B' train SI pump was

considered to have been operable based on the time of the last successful run and the

observed accumulator level trends which indicated insufficient leakage to fill the Unit 1

'B' SI pump with nitrogen-saturated water leading to gas binding failure as had occurred

with 2P-15B.

Concerns for voiding of common ECCS piping were eliminated due to elevation

differences between the SI pump casings and other ECCS pump common suction lines

(the SI pump casings were 3.5 feet above the common ECCS suction line), the fact that

the adjacent pump (2P-15A) exhibited no symptoms of gas binding, and the likelihood

that at least a portion of the evolved gas had been venting through the 2P-15B pump

shaft seals. The inspectors also reviewed the effect of the SI flow delay to the reactor

core during design transients caused by partially voided injection lines and determined

that the limiting parameter of concern, nuclear fuel peak centerline temperature,

remained bounded by existing accident analyses. A review of the gas voiding on water

hammer, shock amplification loadings, valve pressure locking, and instrumentation

effects raised no other operability concerns.

9

Analysis

The inspectors assessed this issue using the Significance Determination Process. The

inspectors concluded that the failure of the 2P-15B SI pump had a credible impact on

safety since the 2P-15B SI pump was credited for mitigating the consequences of

design basis and risk significant transients including: reactor trips, transients without the

secondary power conversion system, loss of a single 125-VDC safeguards bus, small

break LOCAs, stuck open pressurizer power-operated relief valves, medium break

LOCAs, loss of offsite power, loss of offsite power plus loss of the gas turbine with one

emergency alternating current power source unavailable, steam generator tube rupture,

and main steam line break accidents. Consequently, the failure of the 2P-15B SI pump

had a credible impact on safety and was associated with the mitigating systems

cornerstone.

Using the Significance Determination Process Phase 1 Screening Worksheet for the

Mitigating Systems Cornerstone, the inspectors concluded that failure of the 2P-15B SI

pump was considered to be at least of very low safety significance (Green). Pending

further inspector and Region III review of the regulatory and risk aspects of the pump

failure, the safety significance of the finding is To Be Determined and this issue will be

considered an Unresolved Item (URI). Problem identification and resolution aspects of

the failure are discussed in Section 4OA2 of this report.

.2 2P-15B SI Pump Failed to Meet Differential Pressure Acceptance Criteria

a. Inspection Scope

The inspectors reviewed OBD 000005, 2P-15B SI Pump Failed to Meet Differential

Pressure Acceptance Criteria, to determine operability following a rebuild of the 2P-15B

SI pump due to a failure caused by gas binding on February 20, 2002. Specifically, the

inspectors reviewed Inservice Test IT-02 High Head Safety Injection Pumps and Valves

(Quarterly) Unit 2, Revision 48, performed on February 24, 2002, to determine the

impact of the 800 gallons per minute flow test point which was found to be below the

acceptance criteria of the FSAR pump curve. The inspectors reviewed the licensee's

position that failure of 2P-15B to meet the SI pump curve defined in FSAR

Figure 14.3.2-13, PBNP High Head Safety Injection Flow, at 800 gallons per minute

constituted an operable-but-degraded condition applicable to the SI pump curve rather

than the SI pump itself. The inspectors reviewed the effects of the reduced SI pump

flow on nuclear fuel peak clad temperatures to verify that existing analyses remained

bounding for all design basis accidents. Finally, the inspectors reviewed licensee plans

to modify the SI pump rotating assembly or revise the FSAR SI pump flow curve to

verify that as-built equipment capabilities were accurately reflected in the design bases.

b. Findings

No findings of significance were identified.

.3 Non-Quality Assurance (QA) Ammeter and Voltmeter Installed In Safety-Related Battery

Chargers

a. Inspection Scope

10

The inspectors reviewed the OBD associated with AR 2432, Non-QA Parts Used in SR

[Safety-Related] Equipment, D-107 Delayed, to understand the impact of a Non-QA

ammeter installed in safety-related battery charger D-109 in August 2000 and a Non-QA

voltmeter installed in safety-related battery charger D-108 in April 2000. The inspectors

interviewed the 125-VDC system engineer and reviewed battery charger FSAR design

basis requirements to determine if failure of the meters could prevent the fulfillment of

any safety-related functions. The inspectors also considered whether design basis

requirements to restore battery chargers to 125-VDC safety-related buses within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />

following a design basis accident, concurrent with loss of offsite power, had been

validated against current emergency and abnormal operating procedures.

b. Findings

No findings of significance were identified.

1R16 Operator Workarounds (OWAs) (71111.16)

.1 Cumulative Effect of OWAs

a. Inspection Scope

Using the OWA list effective on March 25, 2002, the inspectors reviewed the cumulative

effect of OWAs to determine the total impact of these workarounds on plant operations.

Specifically, the inspectors considered the interactions between OWAs associated with

emergency diesel generator (EDG) starting air systems, manual operator action

required to reseat crossover steam dump valves, safety-related battery room ventilation

fan high air flow velocities resulting in water on electrical equipment, air ejector radiation

monitor sensitivity to increasing turbine hall temperatures, direct current bus

over/undervoltage alarms during routine starts of Units 1 and 2 safeguards pumps,

frequent condenser water box level alarms while on ice melt operation, and the frequent

venting of SI pumps and piping due to back-leakage past check valves between the SI

accumulators and the refueling water storage tank on the operator's ability to implement

abnormal and emergency operating procedures. The inspectors also reviewed OWA

meeting minutes from October 2001 to March 2002 to verify that the licensee had been

conducting periodic reviews of OWAs and considering the total impact of workarounds

on plant operations. The inspectors reviewed probabilistic risk assessment personnel

involvement in the periodic workaround reviews to verify that the licensee was

attempting to gain risk insights concerning the cumulative effect of OWAs.

b. Findings

No findings of significance were identified.

.2 Condenser Air Ejector Radiation Monitors Trend Upward With Increasing Turbine Hall

Temperatures

a. Inspection Scope

11

The inspectors reviewed OWA 0-00C-002 RMS [Radiation Monitoring System] to

identify potential effects on the ability of operators to respond to steam generator tube

rupture events and implement abnormal and emergency operating procedures. The

workaround concerned the Units 1 and 2 condenser air ejector radiation detectors

which, during normal operations, were operating at less than 0.005 percent of full scale.

Due to the low alarm setpoint and the low number of detector ionizing events associated

with the detectors, normal seasonal temperature changes in the turbine building

frequently caused detector alarms. The inspectors interviewed radiation protection

personnel to review plans to change procedures to adjust the background constant for

the detectors. The inspectors reviewed design basis transient analysis to verify that the

proposed changes were bounded by existing steam generator tube rupture analyses

and to verify that the operators ability to rapidly detect steam generator tube ruptures

would not be comprised by the proposed changes. In addition, the inspectors verified

that the proposed changes would allow operators to detect steam generator tube leaks

that were well below TS RCS leakage limits. Finally, the inspectors performed limited

walkdowns of the air ejector discharge piping to verify that turbine hall ambient

temperature changes were the only external factor influencing detector count rates.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing (71111.19)

.1 EDG G-02 Post-Maintenance Testing Following Electrical Generator Rotor Rewinding

a. Inspection Scope

The inspectors observed portions of maintenance activities for the G-02 generator

replacement. Subsequently, the inspectors reviewed design basis requirements and

observed portions of the G-02 load capacity tests performed in accordance with Point

Beach Test Procedure 110, Emergency Diesel Generator G-02 Test, Revision 0, to

verify that the G-02 EDG was capable of performing its design and licensing basis

functions. The inspectors reviewed the completed test documentation to verify that all

acceptance criteria had been met. The inspectors also reviewed design basis

requirements and completed documentation for TS Procedure TS-82, Emergency

Diesel Generator G-02 Monthly, Revision 62, to verify operability and configuration of

the EDG G-02. Finally the inspectors reviewed AR 2403, G-02 Intra-Pole Connecting

Strap Installed Improperly, which discussed the improper installation of one of seven

straps that connected the eight rotor poles in series, to evaluate the rigor of the quality

assurance organization oversight that had been applied to the 10 CFR Part 50,

Appendix B, certified vendor that had rewound the EDG rotor.

b. Findings

No findings of significance were identified.

.2 Replacement of 'C' Service Water (SW) Pump Parts Following Vibration Level Increase

12

a. Inspection Scope

The inspectors observed post-maintenance testing activities conducted in accordance

with WOs 0203115 and 0202837 and Inservice Test IT 07C, P-32C Service Water

Pump (Quarterly), Revision 10, following replacement of the 'C' SW pump wearing

rings, column bolting, spider bearings, shafts, and packing glands to verify that the tests

were adequate for the scope of the maintenance work which had been performed and

that the testing acceptance criteria were clear and demonstrated operational readiness

consistent with design and licensing basis documents. The inspectors observed

portions of the pump replacement activities and reviewed completed maintenance and

test records to verify that foreign material exclusion controls were properly applied;

inservice leak tests were properly performed; pump and motor vibrations following

reassembly were at acceptable levels; motor power supply lugs and cables were

properly reattached and assembled; the motor had acceptable electrical performance

characteristics; and shaft runout and bearing clearances following reassembly were

within acceptable limits. The inspectors also reviewed the safety evaluation screening

used to re-baseline the SW pump performance characteristics to verify that all design

basis and American Society of Mechanical Engineers Code requirements were satisfied

for the new pump assembly. Finally, the inspectors reviewed AR 2327, Motor Purchase

Without Recommended Accessory, which discussed a stabilizer bushing sold by the

motor vendor that was not installed during 'C' SW pump modifications activities.

b. Findings

No findings of significance were identified.

.3 EDG G-01 Post-Maintenance Testing Following Limited Maintenance Window

a. Inspection Scope

The inspectors reviewed design basis requirements and observed post-maintenance

testing performed in accordance with Technical Specification Test (TS) 81, Emergency

Diesel Generator G-01 Monthly, Revision 62, to verify operability of the Unit 1 'A' train

EDG following a limited maintenance window which had deferred selected vendor

recommended inspections while replacing engine oil filters. Completed surveillance test

documentation was reviewed to verify that the EDG satisfied all required acceptance

criteria and remained capable of performing the intended safety functions. The

inspectors also reviewed selected safety evaluations to verify that the delayed

maintenance did not increase the probability of occurrence of a malfunction of

equipment important to safety that was described in the current licencing basis. Finally,

the inspectors verified that the deferred maintenance inspections had been entered into

the licensee's work planning program and scheduled for completion within 90 days of

the original inspection date.

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications (71111.23)

13

.1 Installing a Stabilizer Bushing for SW Pump P-32C-M

a. Inspection Scope

The inspectors reviewed Temporary Modification TM 02-006, Steady Bushing for

P-32C-M, to verify that the modification was properly installed, had no effect on the

operability of the safety-related equipment, and adequately reduced vibration levels.

The inspectors observed SW pump testing and associated vibration measurements

after the installation of the temporary modification to ensure that the pump was capable

of performing its intended safety function.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification (71151)

Cornerstones: Initiating Events, Mitigating Systems

.1 RHR System Unavailability PI

a. Inspection Scope

The inspectors reviewed portions of the Units 1 and 2 1999, 2000, and 2001 data for the

RHR System Unavailability PIs using the definitions and guidance contained in Nuclear

Energy Institute 99-02, Regulatory Assessment Indicator Guideline, Revision 2.

The inspectors reviewed station log entries, Licensee Event Reports, selected inservice

text procedures, and system engineer data sheets to verify that planned and unplanned

unavailability hours were characterized correctly in determining PI results. The

inspectors also performed independent calculations to verify PI data.

b. Findings

No findings of significance were identified.

14

.2 Unplanned Power Changes Per 7,000 Critical Hours PI

a. Inspection Scope

The inspectors reviewed Units 1 and 2 2001 data for the Unplanned Power Changes per

7,000 Critical Hours PI using the definitions and guidance contained in Nuclear Energy

Institute 99-02, Regulatory Assessment Indicator Guideline, Revision 2.

The inspectors reviewed station log entries, Licensee Event Reports, and licensee

quarterly data tracking sheets for unplanned power changes greater than 20 percent of

full power to verify that all power changes were properly characterized as planned or

unplanned in determining the PI results. The inspectors also performed independent

calculations to verify PI data.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 2P-15B SI Pump Failure Due to Gas Binding During Monthly Lubrication Run

a. Inspection Scope

The inspectors reviewed the corrective action and operating experience program history

surrounding the self-revealing failure of the 2P-15B Unit 2 SI pump due to gas binding

on February 20, 2002. Specifically, the inspectors reviewed the corrective action and

operating experience history provided by the licensee in Root Cause Evaluation 000044,

Unit 2 Safety Injection Pump Damaged During Routine Preventative Maintenance, to

determine the causes of the 2P-15B failure. A description of the circumstances and

operability considerations associated with the safety injection pump failure are provided

in Section 1R15.1 of this report.

b. Findings

The licensee initiated a root cause evaluation team on February 23, 2002, to identify

why the safety injection pump failure had occurred and to determine corrective actions

to prevent reoccurrence. The licensee's evaluation identified that plant staff had not

properly responded to adverse SI accumulator trends that increased the potential for

gas binding of the SI pumps. The licensee also concluded that the operating experience

program had not been effective in ensuring timely implementation of corrective actions

from previous lessons learned.

The inspectors reviewed the corrective action and operating experience history collected

by the root cause evaluation team and noted at least two specific opportunities for the

licensee to have identified the Unit 2, 'A' accumulator, 2T-34, adverse leakage trend

prior to the 2P-15B SI pump failure.

15

initiated on January 15, 2002, by a licensed reactor operator who identified an

adverse trend in the rate of decrease of the Unit 2 'A' accumulator level. The

operator recommended further evaluation to pinpoint a leakage path since his

analysis efforts had been inconclusive. He attached a graph of the accumulator

level history to the AR which showed a marked increase in the accumulator

leakage rate following performance of the last quarterly 2P-15B TS surveillance

test on December 29, 2001. Prior to December 29, accumulator level had been

decreasing at a rate of approximately 1 percent per day. However, following the

quarterly surveillance test and fill of the accumulator on December 29, the

average rate was 4 to 5 percent per day.

Action Request 1862 was reviewed by plant management on January 16, 2002,

and closed, with no further action, to an open WO to investigate leakage through

the accumulator fill valve.

  • Condition Report 01-0454, Unit 2 'A' Safety Injection SI Accumulator Level, was

initiated on February 12, 2001, by a different licensed reactor operator who

identified that the Unit 2 'A' accumulator level was lowering slowly, requiring

refilling numerous times per OI-100, Adjusting SI Accumulator Level and

Pressure. Work Order 9935625 was initiated to determine whether the

accumulator drain valve, 2SI-844A, or the accumulator fill valve, 2SI-835A, was

leaking. Results of WO 9935625 were inconclusive and CR 01-0454 was closed

to WOs 9939167 and 9939168 to correct the drain and fill valve seat leakage

during the next refueling outage. In closing CR 01-054, the system engineer

noted that either both the drain and fill valves were leaking or another drain path

existed. At the time of the 2P-15B SI pump failure, the WOs to repair the

accumulator fill and drain valves had not yet been completed and remained

open.

Several other Unit 1 and 2 corrective program opportunities had existed to cause the

licensee to question accumulator leakage paths and the consequences of continued

leakage on SI pump operability. Condition Reports 97-1044, Unit 1 SI Accumulator

Stop Valves Leak By; CR 96-0908, Unit 1 SI Accumulator Level Loss; CR 98-0171,

2SI-843B SI Accumulator First Off Isolation Valve Leaking; and CR 99-2717 identified

various combinations of leaking accumulator drain, local sample isolation, and fill valves.

Each CR was closed to a WO which repaired the leaking valves. Other corrective action

program opportunities that had existed and should have caused the licensee to more

thoroughly question potential accumulator leakage paths and the Unit 1 and 2 leakage

consequences included;

initiated on December 17, 1996, and identified that the Unit 1 SI accumulator had

been decreasing about 1 percent per day. The CR was closed to WO 94893

which, at the end of this inspection period, had not been traced to closure in the

licensees work planning system.

  • Condition Report 97-3942, Unit 1 'A' SI Accumulator Lost 86.6 Gallons of

Borated Water, was initiated on December 1, 1997, and identified that the

16

leakage, following evaluation, was believed to be going through fill valve,

1SI-835A. The CR was closed to WO 9714938 which identified that the

accumulator continued to leak even when the drain valve, 1SI-844A, was

isolated. The CR indicated that because of the leakage investigation done, and

other actions in place under CR 97-3932, the only additional action needed was

the creation of a new item for engineering personnel to evaluate if the noted rate

of level increase in the reactor coolant drain tank was acceptable. This action

item had not been created when the CR was closed.

  • Condition Report 98-1004, SI Accumulator Level Decrease, was initiated on

March 11, 1998, and identified that the Unit 2 'A' accumulator was decreasing by

approximately 3 percent per day. The initial recommendation was to close this

CR to an open WO written to repair seat leakage on the 2T-34A accumulator

outlet valve, 2SI-841A. At the request of the system engineer, however, the CR

was re-opened to evaluate and track the issue of dissolved nitrogen coming out

of solution once it had leaked by the accumulator isolation valve. Condition

Report 98-1004 contained a September 1999 cross-reference to OE at another

commercial pressurized water reactor which discussed gas binding of high-head

SI pumps via back-leakage through check valves that isolate the RCS from the

SI and RHR systems.

In addition, several industry OE opportunities had existed to alert the licensee to

examine SI accumulator leakage paths and the potential SI pump operability

consequences. Operating experience opportunities included:

Back-Leakage From Safety Injection Tanks, was evaluated by the license in

September 1997. As a result of the review, Operating Procedure OP-1A, Cold

Shutdown to Hot Shutdown, was revised to require venting of the high point of

the accumulator discharge lines prior to startups.

Injection Pumps During a Loss-of-Coolant-Accident, Supplements 1 through 4,

were evaluated between January 1989 and May 1993. These supplements

focused on gas binding of the high head SI pump suction due to back-leakage

from the RCS and RHR systems.

Injection Pumps During a Loss-of-Coolant-Accident, Supplement 5, and

licensee OE document 9876, 4B HHSI [High-Head Safety Injection] Pump Gas

Binding, were evaluated by the licensee in June 1999. During the evaluation,

the licensee concluded that previous OE responses on the gas binding subject

were incomplete, not thorough, and too narrowly focused, and that the potential

for nitrogen accumulation in the SI piping from check valve or multiple valve

leakage paths had not been addressed. This conclusion resulted in the

generation of a single action item under IN 88-023 for the performance of an

in-depth re-evaluation of the gas binding phenomena, including re-evaluation of

all prior documents on the gas binding issue. The inspectors noted that a CR

17

concerning the lack of rigor of the previous OE responses was not initiated

during the processing of IN 88-023, Supplement 5.

The IN 88-023 action was created in September 1999, and assigned to an

engineer for further evaluation and completion by January 2000. One due date

extension was granted and the evaluation was competed during April 2000. In

the evaluation, the engineer concluded that the SI system was susceptible to gas

binding in the event of leakage from the SI accumulators through multiple check

valves and/or motor-operated valves. In addition, the engineer concluded that,

Frequent filling of an accumulator can be evidence of check valve leakage, and

Small leakage over time can result in gas coming out of solution and voiding

significant amounts of ECCS piping. The engineer recommended that another

action item be created to address these concerns and listed specific areas to be

addressed including:

  • Addition of guidance to OI-100, Adjusting SI Accumulator Level and

Pressure, to check for ECCS piping voids when frequent accumulator

filling was required

  • Consideration of adding frequent venting of the ECCS piping upstream of

the first- and second-off RCS check valves

Discussions between engineering and operations personnel concerning

OI-100 procedure changes occurred between June 2000 and December 2001.

At the beginning of December 2001, an action item was initiated to complete

OI-100 revisions by March 8, 2002. The OI-100 revision had not been issued

prior to the gas binding failure of 2P-15B on February 20, 2002.

In reviewing the corrective action program history of the in-depth re-evaluation of

the gas binding phenomena for the single action item associated with IN 88-023,

Supplement 5, the inspectors noted eight due date extensions encompassing

18 months (June 2000 to December 2001) before operations personnel agreed

to the recommended OI-100 revisions and the revision date of March 8, 2002,

was agreed upon. During the intervening 18 months, the inspectors noted

deferral of OI-100 revisions for changes in system engineers, conflicts with a

Unit 2 refueling outage, assignment of a new system engineer, further research

on the feasibility of corrective actions, evaluation of the impact of improved TSs

on the planned revision, and operations review of the recommended changes.

Pending further regulatory review, this issue will be carried under the URI opened in the

2002 Problem Identification and Resolution Inspection Report 50-266/02-03(DRP);

50-301/02-03(DRP) as URI 50-301/02-03-01.

18

4OA6 Meetings

Exit Meeting

The resident inspectors presented the routine inspection results to Mr. M. Warner and

other members of licensee management at the conclusion of the inspection on

April 5, 2002. The licensee acknowledged the findings presented. No proprietary

information was identified.

Interim Exit Meeting

Senior Official at Exit: N/A. Phone call with Ms. F. Flentje

Date: January 23, 2002, via telephone

Proprietary (explain yes) No

Subject: Results of an licensee investigation on failure to

follow a work order.

Change to Inspection Findings: No

4OA7 Licensee-Identified Violations

The following finding of very low significance was identified by the licensee and is a

violation of NRC requirements which meets the criteria of Section VI of the NRC

Enforcement Policy, NUREG-1600 for being dispositioned as a Non-Cited Violation

(NCV).

If you deny the NCV, you should provide a response with the basis for your denial,

within 30 days of the date of this inspection report, to the Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies

to the Regional Administrator, Region III; the Director, Office of Enforcement, United

Stated Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC

Resident Inspector at the Point Beach facility.

NCV Tracking Number Requirement Licensee Failed to Meet

NCV 50-266/02-05-01 10 CFR Part 50, Appendix B, Criterion V, Instructions,

Procedures, and Drawings, required, in part, that activities

affecting quality be prescribed by documented instructions,

procedures, or drawings of a type appropriate to the

circumstances and shall be accomplished in accordance

with these instructions, procedures, or drawings. Contrary

to the above, on March 27, 2001, electricians commenced

work on the 125-VDC system without authorization from

the Duty Shift Superintendent as required by Work

Order 9928468. In addition, the workers went beyond the

scope of the work order and performed work in an

energized 125-VDC panel. These two issues, combined,

constituted a violation of more than minor significance

because the issues could be viewed as a precursor to a

significant event. Since this finding did not result in a loss

19

of safety function, the inspector determined that, through

the use of Significance Determination Process Phase 1

Screening Worksheet, the issues were of very low safety

significance (Green). These two issues were described in

the licensees corrective actions program as Condition

Reports 01-1073 and 01-1029. This is being treated as a

Non-Cited Violation.

20

KEY POINTS OF CONTACT

Licensee

J. Anderson, Production Planning Group Manager

L. Armstrong, Design Engineering Manager

C. Arnone, Outage Manager

A. Cayia, Site Director

F. Flentje, Senior Regulatory Compliance Specialist

D. Gehrke, Nuclear Oversight Supervisor

N. Hoefert, Engineering Programs Manager

R. Hopkins, Nuclear Oversight Supervisor

V. Kaminskas, Maintenance Manager

C. Krause, Regulatory Compliance

R. Mende, Director of Engineering

D. Schoon, Operations Manager

R. Pulec, Site Assessment Manager

D. Shannon, Radiation Protection Supervisor

C. Sizemore, Training Supervisor

P. Smith, Operations Training Supervisor

J. Strharsky, Assistant Operations Manager

T. Taylor, Plant Manager

S. Thomas, Radiation Protection Manager

R. Turner, Inservice Inspection Coordinator

P. Walker, Training Manager

M. Warner, Site Vice-President

T. Webb, Licensing Manager

NRC

D. Spaulding, Point Beach Project Manager, NRR

ITEMS OPENED, CLOSED, AND DISCUSSED

Open

50-266/02-05-01 NCV Failure to follow work order instructions for initiating work and

performing work beyond the scope of authorization. (Section

4OA7)

Closed

50-266/02-05-01 NCV Failure to follow work order instructions for initiating work and

performing work beyond the scope of authorization. (Section

4OA7)

Discussed

50-301/02-03-01 URI 2P-15B Safety Injection Pump Failure During Monthly

Preventative Maintenance Lubrication Activity (Section 1R15.1)

21

LIST OF ACRONYMS USED

AR Action Request

CFR Code of Federal Regulations

CL Checklist

CR Condition Report

CS Containment Spray

DRP Division of Reactor Projects

ECCS Emergency Core Cooling System

EDG Emergency Diesel Generator

FSAR Final Safety Analysis Report

IN Information Notice

IT Inservice Test

LOCA Loss-of-Coolant-Accident

NRC Nuclear Regulatory Commission

OBD Operability Determination

OE Operating Experience

OI Operating Instruction

OP Operating Procedure

OWA Operator Workaround

PI Performance Indicator

QA Quality Assurance

RCS Reactor Coolant System

RHR Residual Heat Removal

SI Safety Injection

SW Service Water

TDAFW Turbine-Driven Auxiliary Feedwater

TS Technical Specification

URI Unresolved Item

VDC Volts Direct Current

WO Work Order 22

LIST OF DOCUMENTS REVIEWED

1R04 Equipment Alignment

Periodic Checks Switch and Breaker Alignment Checks Revision 32

43 Part 2

0-TS-EP-001 Weekly Power Availability Verification Revision 2

Safety Evaluation Revision of TS-EP-001 and PBF-2035 To March 8, 2002

SCR 2002-0090 Incorporate Revised Bus Voltage Limits

FSAR 8.6.3 120 VAC [Volts Alternating Current] June 2001

Instrument Power (Y)

AR 2652 PC-43 Part 2 March 22, 2002

Master Data Book D-31, DC [Direct Current] Distribution Revision 10

(MDB) 3.2.12

MDB 3.2.12 D-41, DC Distribution Revision 9

Point Beach Drawing Connection Diagram Instrument Rack C207 Revision D

E-94 Sheet 140

Point Beach Drawing Internal Wiring Diagram Local Instrument Revision E

PBE-174 Rack C207

Nuclear Work Order P-29 AFP [Auxiliary Feedwater Pump] Recirc September 11, 1992

(WO) 924198 Control Solenoid

Task Sheet 0009750 Unit 2 Aux Feedwater System Check October 1, 1993

Valves/Flow Indicator

Tag Series 2AF-4002 2P-29 AFP [Auxiliary Feedwater Pump] Mini March 25, 2002

IC Rev1-2 Recirc Control

WO 0200356 2P-29 AFP Mini Recirc Control, Add Backup February 28, 2002

Air to AF-4002

Plant TDAFP [Turbine-Driven Auxiliary Feedwater January 2, 2002

Modification/Minor Pump] Mini Recirc Valve (1/2AF-4002)

Change 02-001 Instrument Air Accumulator Addition

Procedure Feedback PC-43 Part 2, Switch and Breaker Alignment March 22, 2002

Request Checks

Operating Procedure Emergency Diesel Generator G-01 Revision 3

(OP) 11A G-01

OP 11A G-02 Emergency Diesel Generator G-02 Revision 4

Checklist (CL) 13E Auxiliary Feedwater Valve Lineup Revision 14

Part 1 Turbine-Driven Unit 2

23

Temporary Change Auxiliary Feedwater Valve Lineup March 11, 2002

2002-0127 Turbine-Driven Unit 2

Safety Evaluation Backup Air Systems for Auxiliary Feedwater January 25, 2002

SCR 2002-0010 Pump Minimum Flow Recirculation Valves

Point Beach Drawing P&ID Auxiliary Feedwater System - Sheet 1 Revision E

Bech 6118 M-217

Point Beach Drawing P&ID Auxiliary Feedwater System - Sheet 2 Revision E

Bech 6118 M-217

1R05 Fire Protection

Fire Hazards Analysis Fire Area A29, Fire Zone 310, Air August 17, 2001

Report Compressor Room

Fire Hazards Analysis Fire Area A01-E, Fire Zone 246, Electrical August 17, 2001

Report Equipment Room - Unit 2

Fire Hazards Analysis Fire Area A26, Fire Zone 307. Battery Room August 17, 2001

Report D-05

1R11 Licensed Operator Qualifications

Simulator Guide 0065 Shutdown Malfunctions #1 Revision 1

Shutdown Emergency Shutdown LOCA Analysis - Unit 2 Revision 2

Procedure (SEP) 2

SEP 2.2 Shutdown LOCA [Loss of Coolant Accident] Revision 7

With RHR [Residual Heat Removal] Aligned

For Decay Heat Removal - Unit 2

1R12 Maintenance Rule Implementation

MTN Rule Coord File 2000 480 VAC Electrical - Maintenance Rule March 26, 2001

T7.2.6 Performance Criteria/Goals

480 VAC Performance Criteria Assessments January, 2002

Since January, 2001

Maintenance Rule Function List for 480 VAC March, 2001

Electrical

Design Basis 480 VAC System Design Basis Document Revision 1

Document DBD-21

Health Physics Testing Supplied Air For Air-Line Revision 15

Implementing Respiratory Equipment

Procedure 4.56

24

Air Compressor Out-of-Service Times -

August 1999 to February 2002

WO 9934911 Document Maintenance Rule System January 28, 2002

Performance Compared to Performance

Criteria in MRLIN

Instrument Air Performance Criteria

Assessments since January, 2001

Work Orders for Instrument Air Initiated or

Completed Between 1/1/200 and 3/7/2002

NPM 2001-0251 2000 Annual Report for the Maintenance March 26, 2001

Rule

1R14 Personnel Performance During Non-Routine Plant Evolutions

OP 3A Power Operation to Hot Standby Revision 58

OP 3B Reactor Shutdown Revision 33

OP 3C Hot Standby to Cold Shutdown Revision 86

AR 2284 Unit 2 Shutdown To Mode 4 Almost Causes February 23, 2002

a UE [Unusual Event] Entry

AR 2285 2RE-109 Went Into Hi Alarm Tonight February 23, 2002

AR 2287 2Re-109 High Alarm Due To Crud Burst February 23, 2002

During Unit 2 Shutdown for 2P-15B SI

Pump Repairs

AR 2289 AOP 8A, High Coolant Activity, Is Unclear February 23, 2002

On When To Restore Normal PAB [Primary

Auxiliary Building] Access

AR 2290 Unexpected Alarm On Radiation Monitor February 23, 2002

RE-109

A2323 U2 N32 Source Range Detector Failure February 26, 2002

With Less Than One Cycle of Operations

AR 2448 Unusual Event Declared on 3-4-02: Lack of March 7, 2002

Plant Guidance

NPM 2002-0116 Point Beach Nuclear Plant Emergency March 7, 2002

Preparedness Response to March 4, 2002 -

Unusual Event, Toxic/Flammable Gas

Intrusion

1R15 Operability Evaluations

25

OBD 000011 Gas Binding of SI [Safety Injection] Pumps February 24, 2002

OBD 00005 2P-15B SI Pump Failed to Meet Differential February 24, 2002

Pressure Acceptance Criteria

Design Basis SI and CS [Containment Spray] System Revision 0

Document DBD 11

Phase 2 Significance Risk-Informed Inspection Notebook for Point November 29, 2000

Determination Beach Nuclear Plant, Units 1 and 2,

Process Worksheets Prepared by Brookhaven National

Laboratory

OI-100 Adjusting SI Accumulator Level and Revision 16

Pressure

OI-163 SI, RHR [Residual Heat Removal], and CS Revision 1

Pump Runs

Inservice Test (IT) High Head SI Pumps and Valves (Quarterly) Revision 48

IT 02 Unit 2

Drawing PB 02 MSIL P&ID Safety Injection System Unit 2 Revision E

000 001 45

Drawing PB 02 MSIL SI Pump Discharge to Injection Unit 2 Revision E

133 002 10 SI-150IR-1 and SI-1501R-3

PB Drawing 02 MSIL SI Pump Discharge to Injection Line Unit 2 Revision E

133 003 10 SI-150IR-1 and SI-1501R-2

Drawing PB 02 MRDL Suction From RWST to SI, CS, RHR Pumps Revision E

183 001 14 Unit 2

Drawing PB 02 MRHL SI RHR System to Reactor Vessel Unit 2 Revision E

183 001 06 6SI-601R-2

Drawing PB 02 MSIL 2" SI Piping in Containment Unit 2 - Sheet 1 Revision E

183 054 00

Drawing PB 02 MSIL 2" SI Piping in Containment Unit 2 - Sheet 2 Revision E

183 055 01

Drawing PB 02 MSIL 2" SI Piping in Containment Unit 2 - Sheet 3 Revision E

183 056 00

Drawing PB 02 MSIK P&ID Safety Injection System Unit 2 Revision E

000 001 48

Drawing PB 02 MSIK P&ID Safety Injection System, Unit 2 Revision E

000 001 49

26

Drawing PB 02 MSIK P&ID Safety Injection System, Unit 2 Revision E

000 002 43

Drawing PB 01 MESK P&ID Safety Injection System, Unit 1 Revision E

000 002 49

Drawing PB 01 MSIK P&ID Safety Injection System, Unit 1 Revision E

000 001 55

Drawing PB 01 MSIK P&ID Safety Injection System, Unit 1 Revision E

00012 45

OPR 000007 QA Classification of Replacement Ammeter March 7, 2002

and Voltmeter for Safety-Related Battery

Charger

FSAR Section 8.7 125 VDC Electrical Distribution System June 2001

(125V)

1R16 Operator Workarounds

Monthly Operator October 2001 to March 2002

Work Around Meeting

Minutes

Operator Work Summary List March 25, 2002

Around Summary

FSAR 14.2.4 Steam Generator Tube Rupture June 2001

OWA 0-00C-002 1 and 2 RE-215 Trends Up With Increasing March 25, 2002

RMS Turbine Hall Temperatures

1R19 Post-Maintenance Testing

Point Beach Test EDG G-02 Test Revision 0

Procedure 110

Technical Emergency Diesel Generator G-02 Monthly Revision 62

Specification Test

(TS)-82

CAP002391 G01 EDG Amber Light Lit When G02 EDG March 5, 2002

Stopped Running

Design Basis Emergency Diesel Generator System Revision 0

Document DBD-16

AR 2403 G-02 Intra-Pole Connecting Strap Installed March 5, 2002

Improperly

IT 07C P-32C Service Water Pump (Quarterly) Revision 10

27

Safety Screening 0P-32C Rebaselining March 7, 2002

SCR 2002-0089

Procedure Change Modification of IT-7C Attachment A Flow March 8, 2002

Request Form Rate Acceptance Criteria Upper Limit From

4790 to 5098 Gallons Per Minute

WO 0203115 Dissassemble/Inspect/Rebuild Pump

Assembly Being Removed and Reinstalled

Under Work Order 0202837

WO 0202837 Dissassemble Pump and Inspect and

Replace Parts as Per RMP [Routine

Maintenance Procedure] 9216-1, 2, 3

RMP 9216-1 Service Water Pump Motor Removal and Revision 3

Installation

RMP 9612-2 Service Water Pump Motor Removal, Revision 3

Installation and Maintenance

RMP 9612-3 Service Water Pump Vibration Testing and Revision 5

Balancing for Post Maintenance Testing

ASME Code Replace Bolting at Column-to-Column March 6, 2002

Repair/Replacement/ Flanges for P-32C Service Water Pump

Modification Form

2002-0018

AR 2326 P32C OOS Due to High Vibrations February 27, 2002

AR 2327 Motor Purchase Without Recommended February 27, 2002

Accessary

AR 2291 EM [Electrical Maintenance] Workplan Had February 24, 2002

Incorrect Data For G-02 Rotor Resistance

Equation

TS 81 Emergency Diesel Generator G-01 Monthly Revision 62

Safety Evaluation TRM [Technical Requirements Manual] October 8, 2001

2001-0056 Section 3.8.3, Standby Emergency Power

Source Inspection

Safety Evaluation Deferral of G-01 Maintenance Inspection Up February 27, 2002

Screening To Three Months Beyond EMD [Electro-

Motive Diesel] Owners Group

Recommended Maintenance Period

28

Preventative G-01 Emergency Diesel Generator - Two March 12, 2002

Maintenance Work Year Maintenance

Order Deferral

Request

Surveillance Work G-01 Emergency Diesel Generator - Two March 12, 2002

Order Interval Year Maintenance

Extension Request

1R23 Temporary Plant Modifications

TM 02-006 Steady Bushing for P-32C-M February 27, 2002

CAP002326 P32C OOS due to High Vibrations February 27, 2002

CAP002327 Motor Purchase Without Recommended Accessory February 27, 2002

NP 7.3.1 Temporary Modifications Revision 12

4AO1 Performance Indicator Verification

NEI 99-02 Regulatory Assessment Performance Indicator Revision 2

Guideline

Point Beach Mitigating System Cornerstone Monthly Revision 0

Form 1650 Unavailability and Verification, LHSI [Low Head

Safety Injection], January to December 2001

IT-03 Low Head Safety Injection Pumps and Valves Revision 43

(Quarterly) Unit 1

IT-40 Safety Injection Valves (Quarterly) Unit 1 Revision43

IT-45 Safety Injection Valves (Quarterly) Unit 2 Revision 43

Spreadsheet Point Beach Units 1 and 2, Initiating Events

Cornerstone Quarterly Tracking Sheet, 1Q99 to

4Q01

4OA2 Problem Identification and Resolution

Root Cause U2 [Unit 2] Safety Injection Pump April 2002

Evaluation 000044 Damaged During Routine Preventative

Maintenance

Operating Instruction Adjusting SI Accumulator Level and Revision 16

(OI) OI-100 Pressure

NRC Information Potential for Gas Binding of High Pressure Supplement 5

Notice 88-23 SI Pumps During a Loss-Of-Coolant April 23, 1999

Accident

29

NRC Information Potential Nitrogen Accumulation Resulting June 26, 1997

Notice 97-40 from Backleakage from SI Tanks

CR 01-0454 Unit 2 A SI Accumulator Level February 12, 2001

AR 2245 2P-15B SI Pump Fails During OI-163 February 20, 2002

Performance

AR 2262 Concerns About Gas Binding of SI Pumps February 21, 2002

and System Leakage

AR 2264 Untimely Implementation of February 21, 2002

Recommendations from Information Notice

88-23, Supplement 5

AR 2292 2P-15B SI Pump Failed IT-02 February 24, 2002

AR 2294 Unit 1 and 2 SI Accumulators Require February 24, 2002

Frequent Filling Due to Check Valve L

AR 2295 SI Pumps and Piping Require Frequent February 24, 2002

Venting

AR 2296 Valves Found Mis-Positioned in Unit 2 February 25, 2002

Containment

AR 2299 Missed Opportunity to Use OE on Safety February 25, 2002

Inject Pump

AR 2325 Venting of CS Pump Suction February 26, 2002

AR 2432 Non-QA Parts Used in SR [Safety-Related] March 6, 2002

Equipment, D-107 Delayed

30