IR 05000266/2020002

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Integrated Inspection Report 05000266/2020002 and 05000301/2020002
ML20220A308
Person / Time
Site: Point Beach  NextEra Energy icon.png
Issue date: 08/06/2020
From: Nestor Feliz-Adorno
Reactor Projects Region 3 Branch 4
To: Strope M
Point Beach
References
IR 2020002
Download: ML20220A308 (20)


Text

August 6, 2020

SUBJECT:

POINT BEACH NUCLEAR PLANT - INTEGRATED INSPECTION REPORT 05000266/2020002 AND 05000301/2020002

Dear Mr. Strope:

On June 30, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Point Beach Nuclear Plant. On July 8, 2020, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at Point Beach Nuclear Plant.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC Resident Inspector at Point Beach Nuclear Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Néstor J. Féliz Adorno, Chief Branch 4 Division of Reactor Projects Docket Nos. 05000266 and 05000301 License Nos. DPR-24 and DPR-27

Enclosure:

As stated

Inspection Report

Docket Numbers: 05000266 and 05000301 License Numbers: DPR-24 and DPR-27 Report Numbers: 05000266/2020002 and 05000301/2020002 Enterprise Identifier: I-2020-002-0035 Licensee: NextEra Energy Point Beach, LLC Facility: Point Beach Nuclear Plant Location: Two Rivers, WI Inspection Dates: April 01, 2020 to June 30, 2020 Inspectors: K. Barclay, Resident Inspector T. Hartman, Senior Resident Inspector B. Jose, Senior Reactor Inspector Approved By: Néstor J. Féliz Adorno, Chief Branch 4 Division of Reactor Projects Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Point Beach Nuclear Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Establish Instructions that Were Appropriate for Isolating Portions of the Residual Heat Removal System Cornerstone Significance Cross-Cutting Report Aspect Section Barrier Integrity Green [H.5] - Work 71111.20 NCV 05000301/2020002-01 Management Open/Closed A finding of very low safety significance (Green) and associated non-cited violation of Title 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, Drawings," was self-revealed for the licensee's failure to establish instructions for activities affecting quality that were appropriate for the circumstances. Specifically, the licensee's instructions for isolating a portion of the residual heat removal (RHR) system while the reactor coolant system (RCS)was in solid plant conditions resulted in an overpressure of the RCS.

Additional Tracking Items

Type Issue Number Title Report Section Status URI 05000301/2015002-01 Auxiliary Feedwater Pump 71111.04 Closed Trip Time Delay Relay Installed Past Evaluated Service Life URI 05000266,05000301/20 Suitability of Reactor 71111.12 Closed 16002-03 Protection System and Engineered Safeguards System Components Particularly Electrolytic Capacitors

PLANT STATUS

Unit 1 began the inspection period at rated thermal power and remained at or near full power throughout the remainder of the inspection period.

Unit 2 began the inspection period shutdown for refueling outage U2R37. On April 4, 2020, Unit 2 was restarted. On April 5, 2020, the unit was synchronized to the grid, and on April 9, 2020, it achieved full power. The unit remained at or near full power throughout the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the coronavirus (COVID-19), resident inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time the resident inspectors performed periodic site visits each week and during that time conducted plant status activities as described in IMC 2515, Appendix D; observed risk significant activities, and completed on-site portions of IPs. In addition, resident and regional baseline inspections were evaluated to determine if all or a portion of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on-site. The inspections documented below met the objectives and requirements for completion of the IP.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of high summer temperatures and increased electrical system demand.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Emergency diesel generator (EDG) G-04 while EDG G-03 was out-of-service on April 27, 2020
(2) EDG G-03 while EDG G-04 was out-of-service on June 2, 2020
(3) 1P-53 motor-driven auxiliary feedwater (MDAFW) train after testing on May 28, 2020
(4) 2P-53 MDAFW train after maintenance on June 16, 2020

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated system configurations during a complete walkdown of the Unit 2 RHR system on May 7, 2020.

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Fire Zone 151 on May 1, 2020
(2) Fire Zones 156/156A on May 1, 2020
(3) Fire Zone 166 on May 21, 2020
(4) Fire Zones 306/307 on May 21, 2020
(5) Fire Zones 225/226 on June 15, 2020

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)

(1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the control room during reactor and plant startup on April 4, 2020.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated simulator training on June 2, 2020.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (1 Sample)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components remain capable of performing their intended function:

(1) Unit 2 RHR train A heat exchanger flow control valve failure on March 30, 2020.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) elevated risk due to G-05 gas turbine generator maintenance on May 13, 2020
(2) elevated risk due to EDG G-04 maintenance on June 4, 2020
(3) Unit 2 elevated risk due to 2P-53 MDAFW pump maintenance on June 15, 2020
(4) Unit 1 elevated risk due to 1P-10A RHR pump maintenance on June 24, 2020

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (5 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) intake louver for EDG G-01 failed to open
(2) two cells of D-06 battery did not meet voltage requirements during charge
(3) instrument equipment room door found bowed
(4) containment pressure transmitters exceed qualified service life
(5) reactor coolant loop flow trip relay found de-energized

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02)

(1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1) EC 289592, Foxboro to NUS Project - Time Domain Modules (Lead/Lag)

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the following post maintenance test activities to verify system operability and functionality:

(1) TS 82, "Emergency Diesel Generator G-02 Monthly," after alternate output breaker replacement on May 12, 2020
(2) IT 08A, "Cold Start of Turbine-Driven Auxiliary Feed Pump and Valve Test (Partial),"

after maintenance on valve operator 1AF-4002-O on May 20, 2020

(3) 0-SOP-VNBI-003, "White/Yellow Battery and Inverter Room Ventilation Normal Operation," after fan maintenance on May 28, 2020
(4) Work order testing of 1P-2A charging pump after suction pressure switch replacement on May 28, 2020
(5) RMP 9043-47A, "Emergency Diesel Generator G-04 Post-Maintenance Run and Testing," on June 10, 2020
(6) Work order testing of 1P-10A RHR pump after maintenance on June 24, 2020

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated refueling outage U2R37 activities from April 1 to April 9, 2020.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01)

(1) 0-PT-FP-002, "Diesel Engine-Driven Fire Pump Functional Test," on May 1, 2020
(2) 2ICP 02.003A, "Reactor Protection System Logic Train A 31 Day Surveillance Test,"

on May 21, 2020

(3) OI 135E, "LHSI Core Deluge Venting Train A Inside Containment Unit 1," on

May 22, 2020 Containment Isolation Valve Testing (IP Section 03.01) (1 Sample)

(1) ORT 27, "Reactor Coolant Pump Seal Return Unit 2," on March 18,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04) ===

(1) Unit 1 (April 1, 2019 - March 31, 2020)
(2) Unit 2 (April 1, 2019 - March 31, 2020)

BI02: RCS Leak Rate Sample (IP Section 02.11) (2 Samples)

(1) Unit 1 (April 1, 2019 - March 31, 2020)
(2) Unit 2 (April 1, 2019 - March 31, 2020)

71152 - Problem Identification and Resolution

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed the licensees corrective action program for potential adverse trends in maintenance rule failure evaluations that might be indicative of a more significant safety issue.

71153 - Followup of Events and Notices of Enforcement Discretion Event Followup (IP Section 03.01)

(1) The inspectors evaluated a plant transient during solid plant conditions and the licensees response on April 2,

INSPECTION RESULTS

Unresolved Item Auxiliary Feedwater Pump Trip Time Delay Relay Installed 71111.04 (Closed) Past Evaluated Service Life URI 05000301/2015002-01

Description:

In the 2015 second quarter integrated inspection report (05000266/2015002; 05000301/2015002), the inspectors identified an Unresolved Item (URI) due to Unit 2 Turbine-Driven Auxiliary Feedwater (TDAFW) Pump Time Delay Relay 2-62/04044 potentially being installed past its recommended 17-year service life. The licensee captured this issue in Action Request (AR) 02056034. The licensees corrective actions included completing a condition evaluation justifying the continued operation of the relay until the next Unit 2 outage, performing an extent of condition review under AR 02214823, and replacing the relay in late 2015 as part of refueling outage U2R34.

Recently, the inspectors reviewing the issue noted the licensees condition evaluation was partially based on data from calibration and testing activities performed every refueling outage and data from surveillance tests performed each quarter. These activities showed satisfactory relay performance and provided a basis to support continued operation of the relay until it was replaced in 2015. The inspectors noted the relay was installed for 17 years, 8 months prior to its replacement. The inspectors also noted the licensee had completed a modification to the plant in 2011, which resulted in this specific TDAFW pump time delay relay no longer performing a safety function. As a result, the inspectors determined the licensees failure to replace this specific TDAFW relay within their established 17-year frequency was minor and did not constitute a failure to meet NRC requirements.

The licensee also performed an extent of condition review under AR 02214823 and found 52 additional time delay relays installed in engineered safety feature systems, AFW system, Essential Bus A05 and the main steam actuation system which needed further review. Most of these relays were being replaced every 12, 15, or 17 years in accordance with the licensees preventive maintenance strategy and based upon the importance of the relay. In 2017, the licensee implemented Preventive Maintenance Change Requests to conservatively replace all Agastat time delay relays every fifth refueling outage (every 7.5 years).

Based on the review of the items mentioned above, the inspectors did not identify any violations of NRC requirements. This URI is closed.

Corrective Action Reference(s): AR 02056034, AR 02214823 Unresolved Item Suitability of Reactor Protection System and Engineered 71111.12 (Closed) Safeguards System Components Particularly Electrolytic Capacitors URI 05000266,05000301/2016002-03

Description:

In the 2016 second quarter integrated inspection report (05000266/2016002; 05000301/2016002), the inspectors identified an Unresolved Item (URI) associated with components in both units reactor protection system (RPS) and engineered safeguards (ESF)system which contained components known to degrade with age. In some cases, these components may have been installed as original plant equipment. The licensee captured this issue in Action Request (AR) 02138501. The licensees corrective actions included completing a prompt operability determination and performing an extent of condition review under AR 02144821.

Recently, the inspectors reviewing this issue noted that the prompt operability evaluation performed by the licensee was supported by surveillance test data and independent testing performed by the licensees test laboratory in Juno Beach, Florida. The surveillance data and test results showed no degradation of the electrolytic capacitors or other components despite their age. The licensee had been refurbishing the components, including electrolytic capacitors of the associated control modules, on a fifteen-year frequency based on Electric Power Research Institute (EPRI) recommendations. When some of the control module components became obsolete, the licensee initiated efforts to replace the RPS control modules. The Unit 2 RPS control modules were replaced in March 2017 under Engineering Change (EC) 286911. The Unit 1 modules were replaced in October 2017 under EC 286909.

The remaining control modules are scheduled to be replaced during future refueling outages under ECs 288281, 288282 and 291338.

Based on the review of the items mentioned above, the inspectors did not identify any violations of NRC requirements. This URI is closed.

Corrective Action Reference(s): AR 02138501, AR 02144821 Failure to Establish Instructions that Were Appropriate for Isolating Portions of the Residual Heat Removal System Cornerstone Significance Cross-Cutting Report Aspect Section Barrier Integrity Green [H.5] - Work 71111.20 NCV 05000301/2020002-01 Management Open/Closed A finding of very low safety significance (Green) and associated non-cited violation of Title 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, Drawings," was self-revealed for the licensee's failure to establish instructions for activities affecting quality that were appropriate for the circumstances. Specifically, the licensee's instructions for isolating a portion of the RHR system while the RCS was in solid plant conditions resulted in an overpressure of the RCS.

Description:

On April 2, 2020, the licensee was performing startup activities after a refueling outage on Unit 2. At the time, the reactor was in Mode 4 with the RCS solid (i.e., a bubble was not present in the pressurizer). The licensee had the charging system (injection) and the letdown system (removal) matched maintaining RCS pressure steady. The letdown system removed water inventory from the RCS through two paths, one direct and one indirect. The direct path, which was the most significant letdown contributor, was the traditional flow path coming from the RCS through the letdown orifices. The smaller indirect path was from the RHR system through a connection downstream of the letdown orifice. While in this condition, the licensee authorized instruction 2RH-RH-716D Repair, "Replace the Stem Bushing on 2RH-716D," to isolate a portion of the RHR system to facilitate planned maintenance.

The isolation was briefed with the operators performing the activity and then the control room was informed that the RHR system would be isolated. The control room was not informed about the specific equipment that would be manipulated to isolate the system. Also, no one questioned how the isolation would affect the system or plant configuration. The operators isolated the system in accordance with the instructions contained in 2RH-RH-716D Repair.

This activity caused the indirect letdown flow path to isolate without a reduction in charging flow that was equivalent to the indirect letdown flow. As a result, RCS pressure increased until a power-operated relief valve (PORV) lifted. Control room operators recognized the pressure transient and reduced charging flow until RCS pressure stabilized. A subsequent review discovered that instruction 2RH-RH-716D Repair was written assuming the plant had a bubble in the pressurizer and that this assumption was not identified as a prerequisite.

Corrective Actions: The licensee took immediate corrective action to lower charging flow to match letdown and stabilize pressure. Additionally, the licensee added caution notes in the equipment database to all the valves that could potentially affect the letdown path to notify future tagout users of the potential operational effects of manipulating these valves.

Corrective Action References: AR 2350894, AR 2362562, RWA 2341341-16

Performance Assessment:

Performance Deficiency: The inspectors determined that the licensee's failure to establish instructions for activities affecting quality that were appropriate for the circumstances was contrary to 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, Drawings,"

and was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Configuration Control attribute of the Barrier Integrity cornerstone and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. Specifically, the licensee altered the configuration of the RHR system in a manner that adversely affected the RCS barrier by lifting a PORV. The PORV lift breached the RCS barrier by opening a drain path to a tank in containment.

Significance: The inspectors assessed the significance of the finding using Appendix G, Shutdown Safety SDP. The inspectors screened the finding against the Barrier Integrity Cornerstone screening questions in Attachment 1, Exhibit 4, and answered "NO" to all ten screening questions. Therefore, the finding screened to very low safety significance (Green).

Cross-Cutting Aspect: H.5 - Work Management: The organization implements a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority. The work process includes the identification and management of risk commensurate to the work and the need for coordination with different groups or job activities. Specifically, the licensee did not implement a process of controlling and executing the work activity to ensure the associated instructions were appropriate for the plant conditions. In addition, the work process did not include coordination with the control room regarding the equipment that would be manipulated.

Enforcement:

Violation: Title 10 CFR 50 Appendix B, Criterion V, "Instructions, Procedures, Drawings,"

states, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings. The licensee established instruction 2RH-RH-716D Repair, "Replace the Stem Bushing on 2RH-716D,"

dated April 1, 2020, to isolate a portion of the RHR system to perform planned maintenance.

Contrary to the above, on April 2, 2020, an activity affecting quality was not accomplished in accordance with documented instructions of a type appropriate to the circumstances.

Specifically, the isolation instructions contained in 2RH-RH-716D Repair were not appropriate when there was not a bubble present in the pressurizer. However, on April 2, 2020, the licensee implemented 2RH-RH-716D Repair when a bubble was not present in the pressurizer resulting in the lifting of a PORV to prevent a low temperature overpressure condition on the RCS.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Observation: Maintenance Rule Functional Failure Assessment Issues 71152 Inspectors performed a semiannual review to identify trends that might indicate the existence of a more significant safety issue. For their review, the inspectors focused on issues, particularly those entered in to the licensee Corrective Action Program (CAP), associated with not evaluating or tracking Maintenance Rule Functional Failures (MRFF)s.

From December 2019 to May 2020, inspectors identified multiple issues related to the evaluation or tracking of MRFFs. Most notably:

  • Action Request 2334093 documented the failure of a radiation monitor to actuate and re-align the control room ventilation system. The licensee evaluated the condition through the MRFF process and concluded that a MRFF had occurred. During a maintenance rule inspection, the resident inspectors found that the MRFF was not counted towards the total number of MRFF for the system. The licensee reviewed the inspectors concerns and concluded that the MRFF was coded incorrectly in the software. The licensee documented the incorrect coding in AR 2350077 and updated the maintenance rule tracking software with the correct information. The updated total MRFF for the system increased from five to six, which reached the licensees administrative warning level of six. The performance criteria of eight was not exceeded.
  • Action Requests 2350536 and 2350547 documented the failure of an RHR valve to reposition when given a signal from the control room. The resident inspector noted that the licensee did not evaluate the failure through the MRFF process. In response to the inspectors concerns, the licensee initiated AR 2359464 and performed a MRFF assessment. The MRFF assessment determined a functional failure did exist.

The inspectors noted that the cases above involved the incorrect tracking and evaluation of equipment failures against their respective maintenance rule performance criteria. In each case, the failure did not require the component or system to be moved from 50.65(a)(2)status to 50.65(a)(1) and therefore, these issues were considered minor.

The inspectors did not identify any findings or violations during their review.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On July 8, 2020, the inspectors presented the integrated inspection results to Mr. M. Strope, Site Director and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection Type Designation Description or Title Revision or

Procedure Date

71111.01 Miscellaneous PBNP-MISO- Nuclear Plant Operating Agreement for Point Beach Nuclear 7

NUC-001 Plant

Procedures NP 2.1.5 Electrical Communications, Switchyard Access and Work 34

Planning

71111.04 Corrective Action AR 1228612 OE15886 - Safety-Related Agastat Relays Were Found In 04/24/2003

Documents Service

AR 1886057 Replacement Of U2 Relays 262-A, 262-B, 2-62/4044 & 06/27/2013

2-62/4044

AR 1989265 U-1 & U-2 AFW Time Delay Relays Replacement Schedule 09/05/2014

AR 2018491 2015 CDBI FSA: Agastat Relay Aging Management 01/14/2015

AR 2056034 NRC Identified Relay Beyond Recommended Replacement 06/23/2015

Date

AR 2214823 CDBI 2017, PMs not Scheduled in Accordance with 07/12/2017

Manufacturer's Recommendations

Drawings 110E029 Sh. 1 P&ID Auxiliary Coolant System 57

110E035 Sh. 1 P&ID Safety Injection System 56

M-209 Sh. 12 P&ID Emergency Diesel Air Starting System 12

M-217 Sh. 1 P&ID Auxiliary Feedwater System 104

M-217 Sh. 2 P&ID Auxiliary Feedwater System 38

M-217 Sh. 3 P&ID Auxiliary Feedwater System 8

M-219 Sh. 1 P&ID Fuel Oil System 51

M-219 Sh. 3 P&ID Fuel Oil System Diesel Generator Building 17

Engineering 2002-0035 Replacement Schedule of the ESF Electronic Time Delay 10/03/2003

Evaluations Relays (ETDR)

Miscellaneous CL 11A G-03 G-03 Diesel Generator Checklist 9

CL 11A G-04 G-04 Diesel Generator Checklist 11

CL 13E Part 2 Auxiliary Feedwater Valve Lineup Motor Driven 57

PMCR 2171365 Replace All Units 1 and 2 Trains A & B Agastat Time Delay 02/08/2017

Relays in ESF Systems Every 5th Refueling Outage

PMCR 2215026 Replace Auxiliary Feed Water Pump Low Suction Pressure 08/09/2017

Agastat Time Delay Relays Every 5th Refueling Outage

PMCR 2221527 Replace Agastat ETR Series Time Delay Relays 162-A, 09/20/2017

Inspection Type Designation Description or Title Revision or

Procedure Date

2-B, 262-A and 262-B Every 5th Refueling Outage

PMCR 2221547 Replace Agastat ETR Time Delay Relays in Safety-Related 09/21/2017

Buses 1A05 and 2A05 Every 5th Refueling Outage

Procedures CL 13E Part 2 Operations Checklist Auxiliary Feedwater Valve Lineup 57

Motor Driven

71111.05 Drawings FPE-015 Electrical Layout Fire Detection System Aux Bldg. Area 5 0

FPE-017 Electrical Layout Fire Detection System Aux Bldg. Area 4 0

Fire Plans PFP-0-CB Pre-Fire Plan Control Building ELEV 8 FT, 26 FT, 44 FT and 2

FT

PFP-0-PAB-26 Pre-Fire Plan Unit 1 & 2 Auxiliary Building 26 Ft 1

PFP-0-PAB-8 Pre-Fire Plan: Primary Auxiliary Building Elevations 8' and 2

Below

Miscellaneous Fire Round Performance Sheets-PAB 05/06/2020

FPTE 2016-010 Detailed Fire Model Report - Fire Compartment 151 Safety 1

Injection Pump Room, EL 8'-0"

FPTE 2016-011 PBNP Detailed Fire Modeling Report - Fire Compartment 1

156 MCC Room - 1B32, EL 8'-0"

Procedures OM 3.27 Control of Fire Protection and NFPA 805 Equipment 72

71111.11Q Miscellaneous PBN LOC 20B Simulator Exercise Guide One Column 0

2S

Procedures OP 1A Cold Shutdown to Hot Standby Unit 2 18

OP 1B Reactor Startup 79

71111.12 Corrective Action AR 02138501 Reactor Protection System DANA Amplifier Electrolytic 06/16/2016

Documents Capacitors

AR 2160866 U2 Failure of TE-406BD OP/OT DT Turbine Runback 10/07/2016

(White)

AR 2350547 2RH-624 Opened with No Flow Response 03/30/2020

AR 2350938 1RH-624 Visual Inspection of Set Screws 04/02/2020

AR 2356561 M&TE OOT MCVT-001 (No Impact To Plant) 05/13/2020

Corrective Action AR 2359462 MRFF Needed For AR 2350547 06/10/2020

Documents AR 2359464 NRC ID: CRs 02350536 and 02350547 Required 06/10/2020

Resulting from Rescreening

Inspection

Engineering EC 286909 Unit 1 Thot/Tcold R/E Conversion Replacement 3

Inspection Type Designation Description or Title Revision or

Procedure Date

Changes EC 286911 Unit 2 Thot/Tcold R/E Conversion Replacement 3

EC 288281 Unit 1 Delta Flux and Delta T SP2 Module Replacement 4

EC 288282 Unit 2 Delta Flux and Delta T SP2 Module Replacement 4

EC 291338 Foxboro to Curis-Wright Implementation 3

71111.13 Corrective Action AR 2356189 NSCA Engineer To Evaluate G-05 Comp Actions For 2020 05/11/2020

Documents Outage

Corrective Action AR 2339461 Door 157 Not Closing Completely Due to Building D/P 12/26/2020

Documents AR 2359452 W-86 Maintenance Not Included in PRA Look Ahead 06/10/2020

Resulting from

Inspection

Miscellaneous Operations Daily Work List 05/13/2020;

06/15/2020;

06/24/2020

PBN Unit 1 and 2 Current Risk Summary Report 05/13/2020;

06/04/2020;

06/15/2020;

06/24/2020

Point Beach Station Unit 1/2 Daily Status Report 05/13/2020;

06/04/2020;

06/15/2020;

06/24/2020

Procedures NP 10.3.7 On-Line Safety Assessment 43

71111.15 Corrective Action AR 2356902 G01 Louver Failed to Properly Operate during TS 81 05/17/2020

Documents AR 2358829 EQ Qual Life of 1/2PT-947/948 CTMT Low & Intmd PR 06/04/2020

Xmtrs

AR 2359748 D-06 Battery Post Equalize: Two Cells Outside Average 06/12/2020

Range

AR 2360991 Found 2RC-1B De-Energized on Relay Status Checks 2ICP 06/25/2020

2.3B

Corrective Action AR 2359937 Door 486 Appears Bowed (NRC Identified) 06/15/2020

Documents

Resulting from

Inspection

Miscellaneous 0019-300-0020 Summary Report - Analysis of Internal Heat Rise Effects On 0

Inspection Type Designation Description or Title Revision or

Procedure Date

Qualified Life of N-E10 Series, DTN2070 and DTN2010

Pressure Transmitters

DG-G11 Environmental Qualification Service Condition 12

EQCK-FOXB-001 Checklist for Environmental Qualification of Foxboro N-E10 5

Series (N-E11, N-E13) Pressure Transmitter

71111.18 Corrective Action AR 2346369 Mode Panel Switches on New NUSI TMD Modules Faulty 02/27/2020

Documents AR 2351694 2TI-407A Blue Channel Setpoint 1 Failure 04/07/2020

AR 2352490 Replace Setpoint 1 Yellow Channel (2TM-404B) 04/13/2020

Drawings CD-6 JOB 10668 Wiring Diagram - Interconnect Reactor Protection System 17

Rack 1-B1 (1C116) Top Unit 1

CD-8 JOB 10668 Wiring Diagram - Interconnect Reactor Control System Rack 16

1-Y1 (1C118) Top Unit 1

Foxboro 10665 Block Diagram Instrument Protection System Delta T Ave - 12

BD-5 Loop B2

Engineering EC 289592 Foxboro To NUS Project - Time Domain Modules (Lead/Lag) 11/25/2018

Changes

Miscellaneous SCR 2019-0024 RPS/ESFAS Module Replacement EOP STPT Changes 03/06/2019

Work Orders WO 40595771 01 2C-116 Install NUS Modules 04/01/2020

71111.19 Corrective Action AR 2354628 HU Performance Event 04/27/2020

Documents

Drawings 499B466 Sh. Elementary Wiring Diagram Charging Pumps 1P-2A 7

316B

Engineering EC 272841 Install Low Pressure Trip on U1 Charging Pumps 11

Changes

Miscellaneous WP 2020-019 Manually place G-05 Gas Turbine on Turning Gear 04/24/2020

Procedures OM 3.22 Operations Work Plans Development 7

Work Orders WO 40651647 01 A52-DHVR1200-54; Breaker Maintenance Per RMP 9366 02/17/2020

WO 40654420 A52-DHVR1200-25 Breaker Maintenance Per RMP 9366 05/12/2020

WO 40655312 W-086 Lubricate Fan Bearings 05/28/2020

WO 40675453 TS-82 Emergency Diesel Generator Operability Test 05/14/2020

WO 40680389 1P-010A Sample and Change Oil as Required 06/24/2020

WO 40706080 1AF-04002-O/Replace Air Supply Hose 05/26/2020

WO 40711832 18M Mechanical Maintenance 06/11/2020

Inspection Type Designation Description or Title Revision or

Procedure Date

WO 40714864 01 1PS-01366A Leaking on Cubicle Floor 05/28/2020

WO 40721018 1A52-66; MOC Switch Needs Adjustment 06/15/2020

71111.20 Corrective Action RWA 2341341-16 Add Caution/Note to Select Equipment IDs 05/07/2020

Documents

Corrective Action AR 2348442 Items Became Loose In a FME Posted Areas During 03/14/2020

Documents Walkdown In Containment

Resulting from AR 2348444 Items Identified During RP and NRC Walkdown 03/14/2020

Inspection

Drawings 110E029 Sheet 1 P&ID Auxiliary Coolant System Unit 2 57

110E035 Sheet 1 Safety Injection System Unit 2 56

499B466 Sheet Elementary Wiring Diagram Reactor Coolant System 7

757B Remote Operated Valve 2RC431C

499B466 Sheet Elementary Wiring Diagram Remote Operated Valves 10

757D

541F445 Sheet 1 P&ID Reactor Coolant System 52

541F445 Sheet 2 P&ID Reactor Coolant System 34

541F445 Sheet 3 P&ID Reactor Coolant System 19

685J175 Sheet 2 Chemical & Volume Control System Unit 2 68

685J175 Sheet 3 Chemical & Volume Control System Unit 2 20

BD-13 Block Diagram - Instrument Reactor Control System 18

Pressurizer Pressure Control Unit 2

Miscellaneous PBNP Shutdown Safety Assessment and Fire Inspection 03/14/2020-

Checklist 04/03/2020

2R37 Shutdown Safety Assessment Daily Snapshot 03/27/2020

Tagout: 2 RH RH-716D Repair 01

Tagout: 2 OP-4D Part 1 RVLIS 01

PBF-5101 Fuel/Insert/Component Movement Authorization: U2R37 03/22/2020

Core Offload

PBF-5101 Fuel/Insert/Component Movement Authorization: U2R37 03/26/2020

Core Reload

TLB-3 Tank Level Book: Pressurizer Relief Tank, T-2 3

Procedures 2-SOP-RH-002 Residual Heat Removal System Operation 13

2RMP 9096-1 Reactor Vessel Head Removal and Installation Using Biach 21

Tensioning System

Inspection Type Designation Description or Title Revision or

Procedure Date

NP 8.4.7 Control of Safe Load Path and Rigging 14

OP 7A Placing Residual Heat Removal System In Operation 56

SLP 2 Safe Load Path and Rigging Manual: Items Lifted By 33

Containment Polar Crane Unit 2

Work Orders WO 40635368 2ICP 4.4-6 LTOP Transmitters Outage Cal 03/23/2020

WO 40711845 2ICP 2.16-2 - OP Mitigation Sys LTOP Req'd < 392 Deg F 03/28/2020

71111.22 Calculations 2010-0010 Acceptance Criteria for GAMP Sentinel Points 2

Corrective Action AR 2356384 Eight PM Credit Dates Not Correct 05/12/2020

Documents

Engineering EC 293776 FP-3715, P-35B Diesel Fire Pump Discharge Relief Setpoint 0

Changes

Procedures WO 40706906 0-PT-FP-002 Diesel Engine - Driven Fire Pump Functional 05/01/2020

Test

Work Orders WO 40635187 ORT 27, RCP Seal Return 03/18/2020

WO 40676295 OPS Perform OI-135E For Unit 1 SI Train A (IN CTMT) 05/22/2020

WO 40717199 2ICP 2.3A - RP logic Test - Train A 05/21/2020

71151 Corrective Action AR 2355260 Wrong Unit 1 RCS Leakrate Submitted for Aug 2019 05/01/2020

Documents

Resulting from

Inspection

Miscellaneous Performance Indicators; Units 1 and 2; Reactor Coolant 04/01/2019-

System Leakage 03/31/2020

Performance Indicators; Units 1 and 2; Safety System 04/01/2019-

Functional Failures 03/31/2020

LI-AA-100-10003 NRC Performance Indicator 3

Procedures NP 5.2.16 NRC Performance Indicators 22

71152 Corrective Action AR 2350077 NRC Identified: MR Evaluation Documentation Discrepancy 03/26/2020

Documents AR 2359464 NRC ID: CRs 02350536 and 02350547 Required 06/10/2020

Rescreening

17