ML021060307

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IR 05000315/2002-002(DRP), IR 05000316/2002-002(DRP), on 02/09-03/31/2002, Indiana Michigan Power Company, D.C. Cook Nuclear Power Plant, Units 1 and 2. Post Maintenance Testing, Surveillance Testing, Performance Indicator Verification
ML021060307
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 04/16/2002
From: Grant G
Division Reactor Projects III
To: Bakken A
American Electric Power Co
References
EA-02-010 IR-02-002
Download: ML021060307 (58)


See also: IR 05000315/2002002

Text

April 16, 2002

EA-02-010

Mr. A. C. Bakken III

Senior Vice President

Nuclear Generation Group

American Electric Power Company

500 Circle Drive

Buchanan MI 49107

SUBJECT: D. C. COOK NUCLEAR POWER PLANT, UNITS 1 AND 2

NRC INSPECTION REPORT 50-315/02-02(DRP); 50-316/02-02(DRP)

Dear Mr. Bakken:

On March 31, 2002, the NRC completed an inspection at your D. C. Cook Nuclear Power Plant,

Units 1 and 2. The enclosed report documents the inspection findings which were discussed on

April 5, 2002, with you and other members of your staff.

This inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report discusses a finding that appears to have low to moderate safety significance. As

described in Section 4OA1.1 of this report, your staff failed to take corrective action to preclude

a repetitive failure of the Unit 2 Turbine Driven Auxiliary Feedwater Pump (TDAFWP), a

significant condition adverse to quality. Specifically, the Unit 2 TDAFWP failed to start on

August 10, 2001, due to the failure of the trip throttle valve latch mechanism to remain engaged

during pump start. On December 13, 2001, your staff obtained information from the trip throttle

valve vendor identifying critical parameters for the trip hook mechanism geometry and

alignment. Your staff failed to promptly perform corrective actions to verify that the Unit 2

TDAFWP trip hook conformed to these critical parameters. Consequently, a second failure of

the Unit 2 TDAFWP occurred on January 18, 2002, due to the failure of the trip throttle valve

latch mechanism to remain engaged during pump start. Subsequent review determined that

the root cause of the August 10, 2001 and January 18, 2002 failures was due to incorrect trip

hook geometry and alignment.

The inadequate engagement of the Unit 2 TDAFWP throttle valve latch mechanism in

August 2001 resulted in a calculated "T/2" fault exposure time of 42 days. The additional failure

of the Unit 2 TDAFWP in January 2002 represented an additional 38 days of "T/2" fault

exposure. Because both of the TDAFWP failures were related, the NRC evaluated the

identified performance deficiencies, including procedure and corrective action weaknesses, as

a single problem identification and resolution issue. This finding was assessed using the

applicable Significance Determination Process as a potentially safety significant finding that

A. Bakken -2-

was preliminarily determined to be White, a finding with some increased importance to safety,

which may require additional NRC inspection. The finding has a low to moderate safety

significance because the resultant 80 day fault exposure time represented an actual loss of

safety function for a single train of auxiliary feedwater for greater than its Technical

Specification allowed outage time and the train would have been unavailable if called upon for

actual mitigation purposes.

The finding also appears to be an apparent violation of NRC requirements and is being

considered for escalated enforcement action in accordance with the "General Statement of

Policy and Procedure for NRC Enforcement Actions" (Enforcement Policy), NUREG-1600. The

current Enforcement Policy is included on the NRCs website at http://www.nrc.gov.

Before the NRC makes a final decision on this matter, we are providing you an opportunity to

request a Regulatory Conference where you would be able to provide your perspectives on the

significance of the finding, the bases for your position, and whether you agree with the apparent

violation. If you choose to request a Regulatory Conference, we encourage you to submit your

evaluation and any differences with the NRC evaluation at least one week prior to the

conference in an effort to make the conference more efficient and effective. If a Regulatory

Conference is held, it will be open for public observation. The NRC will also issue a press

release to announce the Regulatory Conference.

Please contact Mr. Anton Vegel at (630) 829-9620 within 10 business days of the date of this

letter to notify the NRC of your intentions. If we have not heard from you within 10 days, we will

continue with our significance determination and enforcement decision and you will be advised

by separate correspondence of the results of our deliberations on this matter.

Since the NRC has not made a final determination in this matter, no Notice of Violation is being

issued for this inspection finding at this time. In addition, please be advised that the number

and characterization of apparent violations described in the enclosed inspection report may

change as a result of further NRC review.

Based on the results of this inspection, one additional finding of very low safety significance

(Green) was identified (See Section 1R22). This issue was determined to be a violation of NRC

requirements. However, because of the very low safety significance and because it has been

entered into your corrective action program, the NRC is treating the issue as a Non-Cited

Violation, in accordance with Section VI.A.1 of the NRC Enforcement Policy. If you contest the

Non-Cited Violation, you should provide a response with the basis for your denial, within

30 days of the date of this inspection report, to the Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, Region III; the Director, Office of Enforcement, United States Nuclear Regulatory

Commission, Washington, DC 20555-001; and the NRC Resident Inspector at the D. C. Cook

facility.

A. Bakken -3-

In accordance with 10 CFR 2.790 of the NRCs "Rules of Practice," a copy of this letter

and its enclosures will be available electronically for public inspection in the NRC Public

Document Room or from the Publicly Available Records (PARS) component of NRCs

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

We will gladly discuss any questions you have concerning this inspection.

Sincerely,

/RA/

Geoffrey E. Grant, Director

Division of Reactor Projects

Docket Nos. 50-315; 50-316

License Nos. DPR-58; DPR-74

Enclosure: Inspection Report 50-315/02-02(DRP);

50-316/02-02(DRP)

cc w/encl: J. Pollock, Site Vice President

M. Finissi, Plant Manager

M. Rencheck, Vice President

Strategic Business Improvements

R. Whale, Michigan Public Service Commission

Michigan Department of Environmental Quality

Emergency Management Division

MI Department of State Police

D. Lochbaum, Union of Concerned Scientists

DOCUMENT NAME: G:\cook\ML021060307.wpd *See previous concurrence

To receive a copy of this document, indicate in the box:"C" = Copy without enclosure "E"= Copy with enclosure"N"= No copy

OFFICE RIII E RIII E RIII E RIII E RIII E RIII

NAME DPassehl SBurgess BClayton BKemker AVegel GGrant

DATE 04/11/02 04/09/02 04/12/02 04/09/02 04/10/02 04/16/02

OFFICIAL RECORD COPY

A. Bakken -4-

ADAMS Distribution:

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U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos: 50-315; 50-316

License Nos: DPR-58; DPR-74

Report No: 50-315/02-02(DRP); 50-316/02-02(DRP)

Licensee: American Electric Power Company

Facility: D. C. Cook Nuclear Power Plant, Units 1 and 2

Location: 1 Cook Place

Bridgman, MI 49106

Dates: February 10 through March 31, 2002

Inspectors: B. Kemker, Senior Resident Inspector

K. Coyne, Resident Inspector

J. Maynen, Resident Inspector

H. Peterson, Senior Engineer (Lead Inspector)

D. McNeil, Senior Engineer

W. Slawinski, Senior Radiation Specialist

Approved by: A. Vegel, Chief

Branch 6

Division of Reactor Projects

1

SUMMARY OF FINDINGS

IR 05000315-02-02(DRP), IR 05000316-02-02(DRP), on 02/09 - 03/31/2002, Indiana Michigan

Power Company, D. C. Cook Nuclear Power Plant, Units 1 and 2. Post Maintenance Testing,

Surveillance Testing, Performance Indicator Verification.

The baseline inspection was conducted by resident and region based inspectors. The

inspectors identified one Preliminary White finding, which was an apparent violation and

one Green finding. The significance of most findings is indicated by their color (Green,

White, Yellow, Red) using Inspection Manual Chapter 0609, "Significance Determination

Process" (SDP). The NRCs program for overseeing the safe operation of commercial

nuclear power reactors is described at its Reactor Oversight Process website at

http://www.nrc.gov/NRR/OVERSIGHT/index.html. Findings for which the SDP does not apply

are indicated by "No Color" or by the severity level of the applicable violations.

A. Inspector Identified Findings

Cornerstone: Mitigating Systems

C TBD. The inspectors identified an Apparent Violation of 10 CFR 50, Appendix B,

Criterion V, "Instructions, Procedures, and Drawings," associated with the

licensees failure to perform adequate maintenance and testing on valve

2-CS-369 (reactor coolant pump seal water heat exchanger to volume control

tank (VCT) shutoff valve). This issue was self-revealed on February 16, 2002,

when the Unit 2 west centrifugal charging pump (CCP) exhibited indications of

gas binding following swap over of the suction source from the VCT to the

refueling water storage tank (RWST).

The inspectors assessed this finding using the Significance Determination

Process. The inspectors concluded that this issue had a credible impact on

safety and was therefore more than a minor concern. In particular, the gas

intrusion into the suction of the running Unit 2 west CCP while aligned to the

RWST impacted the capability of the high head injection system to provide the

inventory and reactivity control safety functions. Additionally, the inspectors

concluded that gas intrusion affecting the west CCP could have reasonably

affected the operability and availability of the redundant Unit 2 east CCP. The

inspectors concluded that this issue degraded the licensees ability to add

inventory to the reactor coolant system with the unit shutdown. The risk

significance of this issue will be determined following completion of a Phase 2

analysis for shutdown risk. The safety significance of this issue is to be

determined (TBD) pending the completion of additional staff review.

(Section 1R19)

C Green. A Non-Cited Violation of 10 CFR 50, Appendix B, Criterion XI, "Test

Control," was identified for the licensees failure to utilize valid acceptance

criteria for stroke time testing the Unit 2 pressurizer power operated relief valves

(PORVs). Specifically, the licensee failed to assure that the correct acceptance

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criteria contained in the applicable design document were incorporated into the

surveillance test procedure used for testing the PORVs.

The inspectors assessed this finding using the Significance Determination

Process (SDP). The inspectors determined that this issue could become a more

significant safety concern if left uncorrected and was therefore more than a

minor concern. Specifically, the failure to adequately perform surveillance

testing with valid acceptance criteria could reasonably result in the failure to

identify degraded or inoperable safety related components. The inspectors also

concluded that this issue could credibly affect the operability of the pressurizer

PORVs, which are mitigating system components under the SDP. The

inspectors determined that, because the as-found stroke times were found within

the correct acceptance criteria, this issue was of very low safety significance.

(Section 1R22)

C Preliminary White. An Apparent Violation of 10 CFR 50, Appendix B,

Criterion XVI, "Corrective Actions," was identified for the licensees failure to take

prompt corrective actions to prevent a repetitive failure of the Unit 2 turbine

driven auxiliary feedwater pump (TDAFWP). Specifically, the Unit 2 TDAFWP

failed to start on August 10, 2001, due to the failure of the trip throttle valve latch

mechanism to remain engaged during pump start. On December 13, 2001, the

licensee obtained information from the trip throttle valve vendor identifying critical

parameters for the trip hook mechanism geometry and alignment and failed to

promptly perform corrective actions to verify that the Unit 2 TDAFWP trip hook

conformed to these critical parameters. Consequently, a second failure of the

Unit 2 TDAFWP occurred on January 18, 2002, due to the failure of the trip

throttle valve latch mechanism to remain engaged during pump start.

The inspectors and Region III Senior Reactor Analysts assessed this finding

using the Significance Determination Process (SDP). A Phase 3 SDP analysis

was performed using insights from the licensees updated Probabilistic Risk

Assessment model. Based on the results of the Phase 3 SDP analysis, the NRC

staff determined that this finding has a low to moderate safety significance

because the resultant 80 day fault exposure time represented an actual loss of

safety function for a single train of auxiliary feedwater for greater than its

Technical Specification allowed outage time and the train would have been

unavailable if called upon for actual mitigation purposes. (Section 4OA1)

B. Licensee Identified Violations

No violations of significance were identified.

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Report Details

Summary of Plant Status:

Unit 1 operated at or near full power for the duration of the inspection period.

Unit 2 was defueled at the beginning of the inspection period for refueling outage U2C13.

Following completion of the refueling outage, the licensee synchronized the unit to the grid on

February 28, 2002 and raised power to approximately 30 percent. The licensee subsequently

reduced power that same day to approximately 2 percent to perform an emergent repair to a

steam generator main steam isolation valve. Following repair to the valve, the licensee

synchronized the unit to the grid on March 1, 2002. The unit operated at or near full power for

the remainder of the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R04 Equipment Alignment (71111.04)

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

Mitigating Systems Cornerstone

C Unit 1 Turbine Driven Auxiliary Feedwater (N Train)

C Unit 1 West Component Cooling Water Train

The inspectors selected these systems based on their risk significance relative to the

mitigating systems cornerstone. The inspectors reviewed operating procedures,

Technical Specification (TS) requirements, Administrative Technical Requirements

(ATRs), system diagrams, and the impact of ongoing work activities on redundant trains

of equipment in order to identify conditions that could have rendered the systems

incapable of performing its intended functions.

b. Findings

No findings of significance were identified.

4

1R05 Fire Protection (71111.05)

.1 Routine Resident Inspector Walkdowns

a. Inspection Scope

The inspectors performed fire protection walkdowns of the following four risk-significant

plant areas:

Mitigating Systems Cornerstone

C Unit 1 Main Steam Valve Enclosure (Zone 33)

C Unit 1 Switchgear Room Cable Vault (Zone 55)

C Unit 1 Auxiliary Cable Vault (Zone 56)

C Unit 1 Refueling Water Storage Tank Pipe Tunnel (Zone 116)

The inspectors verified that fire zone conditions were consistent with assumptions in the

licensees fire hazard analysis. The inspectors walked down fire detection and

suppression equipment, assessed the material condition of fire control equipment, and

evaluated the control of transient combustible materials.

b. Findings

No findings of significance were identified.

.2 Temporary Instruction 2515/146, Hydrogen Storage Locations

a. Inspection Scope

The inspectors walked down the licensees bulk hydrogen storage locations to verify that

the licensee was complying with applicable codes and to ensure that unrecognized

conditions do not exist. Additionally, the inspectors reviewed documents and discussed

hydrogen storage locations with engineering personnel.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification (71111.11)

.1 Facility Operating History

a. Inspection Scope

The inspectors reviewed the plants operating history from January 2001 through

January 2002, to assess whether the Licensed Operator Requalification Training

(LORT) program had addressed operator performance deficiencies noted at the plant.

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b. Findings

No findings of significance were identified.

.2 Licensee Requalification Examinations

a. Inspection Scope

The inspectors performed a biennial inspection of the licensees LORT program. The

inspectors reviewed the annual requalification operating and written examination

material to evaluate general quality, construction, and difficulty level. The operating

portion of the examination was inspected during March 27-28, 2002. The operating

examination material consisted of two dynamic simulator scenarios and five job

performance measures (JPMs). The biennial written examination was administered on

March 28, 2002. The biennial written examination consisted of 37 open reference

multiple choice questions. The inspectors reviewed the methodology for developing the

examinations, including the LORT program two year sample plan, probabilistic risk

assessment (PRA) insights, level of difficulty, and previously identified operator

performance deficiencies. The inspectors assessed the level of examination material

duplication during the current year annual examinations and with last years annual

examinations. The inspectors also interviewed members of the licensees management,

and training staff and discussed various aspects of the examination development.

b. Findings

No findings of significance were identified.

.3 Licensee Administration of Requalification Examinations

a. Inspection Scope

The inspectors observed the administration of the requalification operating test to

assess the licensees effectiveness in conducting the test and to assess the facility

evaluators ability to determine adequate performance using objective, measurable

performance standards. The inspectors evaluated the performance of 12 licensed

operators for one operating shift crew during two dynamic simulator scenarios in parallel

with the facility evaluators. The operating shift was divided into three simulator shift

crews for evaluation purposes. Each evaluation crew consisted of two Senior Reactor

Operators, two Reactor Operators, and a Shift Technical Advisor. In addition, the

inspectors observed licensee evaluators administering five JPMs on a select number of

operators. The inspectors observed the training staff personnel administering the

operating test, including pre-examination briefings, observations of operator

performance, individual and crew evaluations after dynamic scenarios, techniques for

JPM cuing, and the final evaluation briefing. The inspectors noted the performance of

the simulator to support the examinations. The inspectors also reviewed the licensees

overall examination security program.

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b. Findings

No findings of significance were identified.

.4 Licensee Training Feedback System

a. Inspection Scope

The inspectors assessed the methods and effectiveness of the licensees processes

for revising and maintaining its LORT program up to date, including the use of feedback

from plant events and industry experience information. The inspectors interviewed

licensee personnel (operators, instructors, training management, and management) and

reviewed the applicable licensees procedures. In addition, the inspectors reviewed the

licensees quality assurance/quality control oversight activities, including licensees

training and department self-assessment reports, to evaluate the licensees ability to

assess the effectiveness of its LORT program and to implement appropriate corrective

actions.

b. Findings

No findings of significance were identified.

.5 Licensee Remedial Training Program

a. Inspection Scope

The inspectors assessed the adequacy and effectiveness of the remedial training

conducted since the previous annual requalification examinations and the training

planned for the current examination cycle to ensure that they addressed weaknesses in

licensed operator or crew performance identified during training and plant operations.

The inspectors reviewed remedial training procedures and individual remedial training

plans, and interviewed licensee personnel (operators, instructors, and training

management). In addition, the inspectors reviewed the licensees current examination

cycle remediation packages for unsatisfactory operator performance on the written

examination and operating test to ensure that remediation and subsequent re-

evaluations were completed prior to returning individuals to licensed duties.

b. Findings

No findings of significance were identified.

.6 Conformance with Operator License Conditions

a. Inspection Scope

The inspectors evaluated the facility and individual operator licensees' conformance with

the requirements of 10 CFR Part 55. The inspectors reviewed the facility licensees

program for maintaining active operator licenses and to assess compliance with

10 CFR 55.53(e) and (f). The inspectors reviewed the procedural guidance and the

7

process for tracking on-shift hours for licensed operators and which control room

positions were granted credit for maintaining active operator licenses. The inspectors

also reviewed eight licensed operators medical records maintained by the facilitys

contracted medical staff for ensuring the medical fitness of its licensed operators and to

assess compliance with medical standards delineated in ANSI/ANS-3.4 and with

10 CFR 55.21 and 10 CFR 55.25. In addition, the inspectors reviewed the licensees

LORT program to assess compliance with the requalification program requirements as

described by 10 CFR 55.59(c).

b. Findings

No findings of significance were identified.

.7 Written Examination and Operating Test Results

a. Inspection Scope

The inspectors reviewed the overall pass/fail results of individual written tests, JPM

operating tests, and simulator operating tests (required to be given per

10 CFR 55.59(a)(2)) administered by the licensee during calender year 2002.

b. Findings

No findings of significance were identified.

.8 Resident Inspector Quarterly Review

a. Inspection Scope

The inspectors assessed licensed operator performance and the training evaluators'

critique during a licensed operator annual requalification evaluation in the D. C. Cook

Plant operations training simulator on March 6, 2002. The inspectors focused on alarm

response, command and control of crew activities, communication practices, procedural

adherence, and implementation of emergency plan requirements.

b. Findings

No findings of significance were identified.

1R12 Maintenance Rule Implementation (71111.12)

a. Inspection Scope

The inspectors evaluated the licensee's implementation of 10 CFR 50.65 (the

Maintenance Rule). The inspectors assessed: (1) functional scoping in accordance

with the Maintenance Rule, (2) characterization of system functional failures, (3) safety

significance classification, (4) 10 CFR 50.65 (a)(1) or (a)(2) classification for system

functions, and (5) performance criteria for systems classified as (a)(2) or goals and

8

corrective actions for systems classified as (a)(1). The inspectors reviewed the

following risk-significant systems and components:

Initiating Events Cornerstone

C Circulating Water System

Barrier Integrity Cornerstone

C Hydrogen Ignitor System

Mitigating Systems Cornerstone

C Compressed Air System

C Component Cooling Water System

In addition, the inspectors reviewed the issues that the licensee entered into its

corrective action program to verify that identified problems were being entered into the

program with the appropriate characterization and significance. The inspectors also

reviewed the licensees corrective actions for Maintenance Rule related issues that were

documented in selected condition reports (CRs).

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed the licensees evaluation and management of plant risk for

maintenance activities on the following equipment:

Mitigating Systems Cornerstone

C Unit 1 East Essential Service Water (ESW) Pump Replacement

C Unit 2 East Centrifugal Charging Pump (CCP) Oil Change and Relay Calibration

C Unit 2 West Component Cooling Water Pump Oil Change

C Unit 1 CD Diesel Generator Outage Maintenance Work Window

These activities were selected based on their potential risk significance relative to the

mitigating systems cornerstone. As applicable for each of the above activities, the

inspectors reviewed the scope of maintenance work, discussed the results of the

assessment with the licensees probabilistic risk analyst or shift technical advisor, and

verified that plant conditions were consistent with the risk assessment. The inspectors

also reviewed TS and ATR requirements and walked down portions of redundant safety

systems, when applicable, to verify that risk analysis assumptions were valid and

applicable requirements were met.

9

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors reviewed the following CRs to ensure that either: (1) the condition did

not render the involved equipment inoperable or result in an unrecognized increase in

plant risk, or (2) the licensee appropriately applied TS limitations and appropriately

returned the affected equipment to an operable status.

Mitigating Systems Cornerstone

C CR 02047050, "Unit 2 West CCP Showed Signs of Air Entrainment"

C CR 02050022, "Control Switch 1-101-NRV-152 May Not Be in the Automatic

Position Fully"

C CR 02057005, "Inability to Test 112 Percent Main Turbine Overspeed Trip

Device"

The inspectors also reviewed the licensees justification for not correcting existing

degraded and nonconforming conditions during refueling outage U2C13 consistent with

the timeliness guidance contained in Generic Letter 91-18, "Information to Licensees

Regarding NRC Inspection Manual Section on Resolution of Degraded and

Nonconforming Conditions," Revision 1.

In addition, the inspectors reviewed the issues that the licensee entered into its

corrective action program to verify that identified problems were being entered into the

program with the appropriate characterization and significance. The inspectors also

reviewed the licensees corrective actions for issues potentially affecting the operability

of structures, systems, and components that were documented in selected CRs.

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications (71111.17)

a. Inspection Scope

The inspectors reviewed the engineering analyses, modification documents and design

change information associated with the following permanent plant modification:

Barrier Integrity Cornerstone

C Design Change 2-DCP-4821, "Install New Impellers In the Containment Spray

Pumps (2-PP-9E & W)"

10

The inspectors verified the design adequacy of the modification and focused the

inspection activities on the following parameters associated with the design change:

heat removal, equipment protection, operations, flowpaths, process media, licensing

basis, and failure modes.

Completed activities associated with the implementation of the modification were also

inspected and the inspectors discussed the modification with the responsible engineers

and operations staff. In addition, the inspectors reviewed the applicable sections of the

TS, Updated Final Safety Analysis Report (UFSAR), and CRs associated with the

design change packages and the installation of the modification.

b. Findings

No findings of significance were identified.

1R19 Post Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed the post maintenance testing requirements associated with the

following scheduled maintenance activities:

Mitigating Systems Cornerstone

C Job Order (JO) 01094018, "Replace Diaphragm in Reactor Coolant Seal Return

to Volume Control Tank Isolation Valve 2-CS-369"

C JO 01262081, "Rebuild the Unit 1 East ESW Pump 1-PP-7E"

C JO 020309004, "Troubleshoot and Repair 2-OME-150-CD, Unit 2 CD Diesel

Generator"

C JO 02049054, "Troubleshoot and Repair 600 Volt Supply Breaker to the Unit 2

CD2 Battery Charger That Tripped Twice"

The inspectors reviewed test methodology and acceptance criteria to assess the

appropriateness of assigned post maintenance testing for the scope of work performed.

Documented test data was reviewed to verify that the testing was complete and that the

equipment was able to perform the intended safety functions.

In addition, the inspectors reviewed the issues that the licensee entered into its

corrective action program to verify that identified problems were being entered into the

program with the appropriate characterization and significance. The inspectors also

reviewed the licensees corrective actions for post maintenance testing related issues

that were documented in selected CRs.

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b. Findings

b.1 Failure to Perform Adequate Maintenance and Testing on Valve 2-CS-369 Resulted in

Gas Binding the Unit 2 West CCP

The inspectors identified an Apparent Violation of 10 CFR 50, Appendix B, Criterion V,

"Instructions, Procedures, and Drawings," associated with the licensees failure to

perform adequate maintenance and testing on valve 2-CS-369 (reactor coolant pump

seal water heat exchanger to volume control tank (VCT) shutoff valve). This issue was

self-revealed on February 16, 2002, when the Unit 2 west CCP exhibited indications of

gas binding following swap over of the suction source from the VCT to the refueling

water storage tank (RWST). Pending additional evaluation, the safety significance of

this issue is "To Be Determined" (TBD).

Description

On February 16, 2002, while performing a vacuum refill of the reactor coolant system

(RCS), control room operators aligned the RWST as the CCP suction source and

isolated the VCT. Following isolation of the VCT, the Unit 2 west CCP exhibited

indications of gas binding, including a drop in pump motor amperage and a reduction of

charging system flow to near 0 gallons per minute (gpm). After operators unisolated the

VCT, the CCP amperage and flow recovered to normal values. Operators then made a

second attempt to swap the CCP suction source from the VCT to the RWST; but again,

the gas binding symptoms returned when the VCT was isolated. Based on the

unexpected system response, the licensee declared the Unit 2 RWST boration flowpath

inoperable and initiated CR 02047050.

The licensee determined that the cause of this event was the failure to have 2-CS-369

fully closed, which, due to the pressure difference between the VCT and the RWST,

allowed gas to vent from the top of the VCT directly to the CCP suction line. The

reactor coolant pump seal return flow can be directed either to the CCP suction via

2-CS-370 or directly to the VCT via 2-CS-369. During normal operation, 2-CS-369 is

sealed closed to prevent VCT cover gas intrusion directly to the CCP suction. On

February 1, 2002, the licensee performed preventative maintenance to replace the

2-CS-369 valve diaphragm under JO 01094018. Because the valve was completely

disassembled to replace the diaphragm, JO 01094018 included instructions for valve

stem stop nut adjustment to ensure that the valve stroke would be correct. Proper

adjustment of the stem stop nut allows full closure of the diaphragm valve without

excessive crushing force on the valve diaphragm. The licensee later identified that the

stem stop nut was incorrectly adjusted, which prevented full closure of the valve.

The inspectors reviewed the maintenance work instructions for the 2-CS-369 diaphragm

replacement and determined that the work instructions were not correctly implemented.

Specifically, maintenance personnel failed to adequately perform the instructions for

valve stop nut adjustment contained in procedure 12 MHP 5021.001.023, "Manual

Diaphragm Valve Maintenance," Revision 6. Steps 6.6.3, 6.6.4, and 6.6.5 of

12 MHP 5021.001.023 required that the stem stop nut be locked in position by

tightening the stem lock nut after the valve was turned clockwise 1/8 of a turn beyond

the closed seat contact point. The purpose of these steps was to ensure that the

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position of the stop nut would allow full closure of 2-CS-369. On February 16, 2002, the

licensee identified that the stem lock nut was loose and that the position of the stop nut

prevented full closure of 2-CS-369. The licensee performed several corrective actions

for this condition, including: (1) adjustment of the stop nut and closing of 2-CS-369;

(2) venting of the safety injection (SI) pump and CCP suction headers; and, (3) testing

of the Unit 2 west CCP in accordance with procedure 02 OHP 4030.STP.052W, "West

Centrifugal Charging Pump Operability Test." The licensee subsequently declared the

RWST boration flowpath operable on February 17, 2002.

In addition, the inspectors determined that the post maintenance testing performed

following diaphragm replacement was not adequate to identify the potential

mis-positioning of the stem stop nut. The post maintenance testing requirements in

JO 01094018 specified only an external leakage inspection. The inspectors noted that

although full closure of 2-CS-369 was required to prevent gas intrusion into the suction

of the CCPs, no testing was performed on 2-CS-369 immediately following diaphragm

replacement to verify valve seat leak tightness. The inspectors determined that the

failure to correctly implement maintenance instructions for valve stem stop nut

adjustment and the failure to perform an adequate post maintenance test constituted a

violation of NRC requirements.

Analysis

The inspectors assessed this issue using the Significance Determination Process

(SDP). The inspectors concluded that this issue had a credible impact on safety and

was therefore more than a minor concern. In particular, the gas intrusion into the

suction of the running Unit 2 west CCP while aligned to the RWST impacted the

capability of the high head injection system to provide inventory and reactivity control

safety functions. Additionally, the inspectors concluded that gas intrusion affecting the

west CCP could have reasonably affected the operability and availability of the

redundant Unit 2 east CCP. Consequently, the inspectors determined that this issue

was associated with the mitigating systems cornerstone. The inspectors concluded that

2-CS-369 was degraded when the diaphragm was replaced (February 1, 2002) until

completion of the corrective action to adjust the valve stem stop nut

(February 16, 2002). Therefore, the inspectors concluded that this issue should be

reviewed using the guidance provided in Inspection Manual Chapter (IMC) 0609,

Appendix G, "Shutdown Operations Significance Determination Process." The

inspectors considered the following during the initial risk assessment:

C The 2-CS-369 diaphragm was replaced on February 1, 2002 with Unit 2

defueled. Unit 2 entered Mode 6 (Refueling) on February 10, 2002 and

completed core reload on February 12, 2002. Because the degraded condition

of 2-CS-369 was identified and corrected on February 16, 2002, the safety

function provided by the CCPs was degraded for approximately 6 days with fuel

in the reactor vessel.

C Based on the observed Unit 2 west CCP performance during the gas intrusion

event on February 16, 2002 (decreased pump amperage and near 0 gpm

flowrate), the inspectors concluded that the degraded condition of 2-CS-369

would render the CCPs unavailable when aligned to the RWST.

13

C The licensee determined that both SI pumps were available during the period,

except for 2-1/2 hours on February 12, 2002. During the time that the SI pumps

were unavailable, the unit was in Mode 6 with refueling cavity level greater than

23 feet above the active fuel level.

C To support low temperature over-pressure protection (LTOP) requirements, the

breakers for both SI pumps were racked out. The licensee estimated that

approximately 30 minutes would be required to restore an SI pump to service.

Use of the SI pumps to restore RCS inventory during a loss of inventory was

addressed in abnormal procedure 02 OHP 4022.017.001, "Loss of RHR

[Residual Heat Removal] Cooling."

C The inspectors determined that gas intrusion into the suction of the CCPs would

not be expected to cause a similar failure for the SI pumps. Although the SI

pumps share a common suction with the CCPs from the RWST, check valve

2-SI-185 would prevent migration of gas to the suction of the SI pumps. The

licensee seat leak tested 2-SI-185 on February 8, 2002 and measured a seat

leakage rate of 0 gpm.

C Based on a review of the Unit 2 shutdown risk status sheets during the period of

February 15 and 16, 2002, the inspectors determined that the minimum time to

boil upon a loss of core cooling was 13 minutes. The time to boil with the reactor

coolant not in a reduced inventory condition was estimated to be approximately

2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />.

C The licensee entered a mid-loop reduced inventory condition on

February 15, 2002 to support vacuum refill of the RCS. The licensee exited the

mid-loop condition on February 16, 2002. The inspectors estimated that the unit

was in reduced inventory condition for approximately 23 hours2.662037e-4 days <br />0.00639 hours <br />3.80291e-5 weeks <br />8.7515e-6 months <br />.

C Because the reactor coolant had not been fully refilled prior to the event, the

steam generators were unavailable for core cooling.

C The remote unit has the capability to provide high head injection via unit cross-tie

valves. Although procedure 02 OHP 4025.001.001, "Emergency Remote

Shutdown," addresses use of the charging system cross-tie during certain

Appendix R fire protection events, it did not include specific instructions for

inventory control during loss of shutdown cooling events.

Based on the above information, the inspectors concluded that the most appropriate

IMC 0609, Appendix G checklist to use for this issue was the checklist for "Pressurized

Water Reactor Cold Shutdown and Refueling Operation - Reactor Coolant System

Closed and No Inventory in Pressurizer, Time to boiling less than 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />." Because of

the unavailability of the high pressure injection CCPs due to the degraded condition of

2-CS-369, the inspectors concluded that the minimum equipment specified in

Section II.C were not met from February 14, 2002 (when the unit entered Mode 5) to

February 16, 2002 (when the licensee identified and corrected the degraded condition of

2-CS-369). Consequently, the inspectors concluded that this issue degraded the

licensees ability to add inventory to the RCS and therefore required a Phase 2 analysis.

14

The risk significance of this issue will be determined following completion of a Phase 2

analysis for shutdown risk. The inspectors discussed the safety significance of this

issue with the Regional Senior Reactor Analysts (SRAs), and, pending the completion of

additional evaluation, the safety significance of this issue is to be determined (TBD).

Enforcement

10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," requires

that activities affecting quality shall be prescribed by documented instructions,

procedures, or drawings, of a type appropriate to the circumstances and shall be

accomplished in accordance with these instructions, procedures, or drawings.

Instructions, procedures, or drawings shall include appropriate quantitative or qualitative

acceptance criteria for determining that important activities have been satisfactorily

accomplished. Contrary to the above, the licensee failed to (1) correctly accomplish the

instructions provided in 12 MHP 5021.001.023, Section 6.6, for valve stroke adjustment

of 2-CS-369, an activity affecting quality, and (2) provide appropriate acceptance criteria

to ensure that valve stop nut adjustment was satisfactorily accomplished. Specifically,

steps 6.6.3, 6.6.4, and 6.6.5, which were performed on February 1, 2002, required that

the handwheel for 2-CS-369 be turned clockwise 1/8 of a turn beyond the point where

the valve made closed seat contact, and the stem stop nut be turned clockwise until it

made contact with the handwheel and then locked in position by tightening the stem lock

nut. On February 16, 2002, the licensee identified that the stem stop nut was not locked

and its position prevented full closure of 2-CS-369, which allowed VCT cover gas to flow

to the CCP suction header. In addition, the instructions provided in JO 01094018 did

not include appropriate acceptance criteria to ensure that 2-CS-369 valve stroke

adjustment had been satisfactorily accomplished after valve maintenance.

Consequently, on February 16, 2002, the Unit 2 west CCP became gas bound following

alignment of the pump suction to the RWST. This issue is considered to be an

Unresolved Item pending a final safety significance determination

(URI 50-316-02-02-01(DRP)).

1R20 Refueling and Outage Activities (71111.20)

a. Inspection Scope

The inspectors continued their evaluation of the licensees conduct of Unit 2 refueling

outage activities during this inspection period to assess the licensees control of plant

configuration and management of shutdown risk. The inspectors reviewed configuration

management to verify that the licensee maintained defense-in-depth commensurate with

the shutdown risk plan and reviewed major outage work activities to ensure that correct

system lineups were maintained for key mitigating systems. Other major outage

activities evaluated included the licensees control of the following:

C Containment penetrations in accordance with the TS

C Systems, structures, and components (SSCs) which could cause unexpected

reactivity changes

C Flow paths, configurations, and alternate means for RCS inventory addition and

control of SSCs which could cause a loss of inventory

C RCS pressure, level, and temperature instrumentation

15

C Switchyard activities and the configuration of electrical power systems in

accordance with the TS and shutdown risk plan

C SSCs required for decay heat removal

The inspectors also observed portions of the restart activities to verify that requirements

of the TS and administrative procedure requirements were met prior to changing

operational modes or plant configurations. Major restart inspection activities performed

included:

C Verification that RCS boundary leakage requirements were met prior to entry into

Mode 4 (Cold Shutdown) and subsequent operational mode changes

C Verification that containment integrity was established prior to entry into Mode 4

C Inspection of the Containment Building to assess material condition and search

for loose debris, which if present could be transported to the containment

recirculation sumps and cause restriction of flow to the emergency core cooling

system (ECCS) pump suctions during loss-of-coolant accident conditions

C Verification that the material condition of the Containment Building ECCS

recirculation sumps met the requirements of the TS and was consistent with the

design basis

C Observation and review of reactor physics testing to verify that core operating

limit parameters were consistent with the core design so that the fuel cladding

barrier would not be challenged

The inspectors interviewed operations, engineering, work control, radiological protection,

and maintenance department personnel and reviewed selected procedures and

documents.

In addition, the inspectors reviewed the issues that the licensee entered into the

corrective action program to verify that identified problems were being entered into the

program with the appropriate characterization and significance. The inspectors also

reviewed the licensees corrective actions for refueling outage issues documented in

selected CRs.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

For the surveillance test procedures listed below, the inspectors observed selected

portions of the surveillance tests and reviewed the test results to determine whether risk

significant systems and equipment were capable of performing their intended safety

functions and to verify that testing was conducted in accordance with applicable

procedural and TS requirements:

16

Barrier Integrity Cornerstone

C 02 OHP 4030.STP.007E, "East Containment Spray System Operability Test"

Mitigating Systems Cornerstone

C 02-OHP-4030-202-060, "Pressurizer Relief Valve Testing"

C 02-OHP 4030.001.002, "Containment Inspection Tours"

C 02-OHP-4030-232-217A, "DG2CD Load Sequencing & ESF Testing"

The inspectors reviewed the test methodology and test results in order to verify that

equipment performance was consistent with safety analysis and design basis

assumptions. The inspectors also reviewed CRs concerning surveillance testing

activities to verify that identified problems were appropriately characterized.

b. Findings

b.1 Failure to Use Valid Acceptance Criteria for Stroke Time Testing the Unit 2 Pressurizer

Power Operated Relief Valves (PORVs)

The inspectors identified a finding of very low safety significance (Green) associated

with the licensees failure to utilize valid acceptance criteria for stroke time testing the

Unit 2 pressurizer PORVs. This finding was dispositioned as a Non-Cited Violation of

10 CFR 50, Appendix B, Criteria XI, "Test Control."

Description

The inspectors examined the results of stroke time testing of the Unit 2 pressurizer

PORVs (2-NRV-152 and 2-NRV-153), which was performed on February 12, 2002 to

obtain new in-service testing baseline stroke time values for the valves following

maintenance and to demonstrate operability of the valves for LTOP prior Unit 2 entering

Mode 5 (Cold Shutdown) upon completion of refueling activities. The two air-operated

valves are provided with backup air supply bottles that are designed to provide sufficient

air to cycle the PORVs for 10 minutes without operator action during an LTOP event.

The minimum backup air supply bottle pressure (900 pound per square inch) and the

minimum valve stroke cycle (open and closed) are therefore critical parameters. The

licensee had previously had difficulty meeting the minimum stroke time acceptance

criteria when testing the valves at the beginning of the Unit 2 refueling outage and

revised the acceptance criteria based on its review of the original design calculation for

sizing the backup air supply bottles. The inspectors compared the acceptance criteria in

the completed surveillance test procedure (02-OHP-4030-202-060, "Pressurizer Relief

Valve Testing," Revision 0, Change 0) with the approved acceptance criteria in Design

Information Transmittal (DIT)-B-02327 and noted that the licensee had failed to correctly

use the revised acceptance criteria. Specifically, DIT-B-02327 determined the following

minimum valve stroke time requirements for both 2-NRV-152 and 2-NRV-153:

17

Open Closed

2.39 seconds minimum 1.33 seconds minimum

or

Open Closed Open + Closed

2.0 seconds minimum 1.0 second minimum 3.72 seconds minimum

The second set of minimum stroke time values were provided in DIT-B-02327 as an

alternative set of acceptance criteria with the stipulation that the sum of the minimum

open and closed times be equal to or greater than 3.72 seconds. Based on the sizing

calculation, the PORVs would not be considered operable if the sum of the minimum

open and closed times was less than 3.72 seconds.

The acceptance criteria used in 02-OHP-4030-202-060 for 2-NRV-152 was:

Open Closed

2.8 seconds minimum 1.0 second minimum

The acceptance criteria used in 02-OHP-4030-202-060 for 2-NRV-153 was:

Open Closed

2.6 seconds minimum 1.0 second minimum

The inspectors first noted that the acceptance criteria used in the surveillance test

procedure for both valves did not match the acceptance criteria specified in

DIT-B-02327. This could be considered acceptable provided the sum of the minimum

open and closed acceptance criteria values for each valve is less than 3.72 seconds.

The inspectors then identified that although the sum of the minimum open and closed

acceptance criteria values used in the surveillance test procedure for 2-NRV-152

(3.8 seconds) was greater than 3.72 seconds, the sum of the minimum open and closed

acceptance criteria values for 2-NRV-153 (3.6 seconds) was less than 3.72 seconds. It

was therefore possible to meet the acceptance criteria used in the surveillance test

procedure for 2-NRV-153 with unacceptable test results and to consider an inoperable

valve to be operable. The inspectors compared the as-found stroke times for the two

valves with the correct acceptance criteria from DIT-B-02327 and concluded that the

valves were operable.

Analysis

The inspectors assessed the licensees failure to utilize valid acceptance criteria for

testing the Unit 2 pressurizer PORVs using the SDP. The inspectors determined that

this issue could become a more significant safety concern if left uncorrected and was

therefore more than a minor concern. The inspectors reviewed the licensees corrective

action program database and were concerned that there were several additional

examples captured in the licensees corrective action program, wherein incorrect

acceptance criteria had been utilized for testing. Specifically, the failure to adequately

perform surveillance testing with valid acceptance criteria could reasonably result in the

failure to identify degraded or inoperable safety related components. The inspectors

18

also concluded that this issue could credibly affect the operability of the pressurizer

PORVs, which are mitigating system components under the SDP. The inspectors

determined that, because the as-found stroke times were found within the correct

acceptance criteria, this issue was of very low safety significance (Green).

Enforcement

10 CFR Part 50, Appendix B, Criterion XI, "Test Control," requires, in part, that a test

program shall be established to assure that all testing required to demonstrate that

structures, systems, and components will perform satisfactorily in service is identified

and performed in accordance with written test procedures which incorporate the

requirements and acceptance limits contained in applicable design documents.

Contrary to the above, the licensee failed to assure that 02-OHP-4030-202-060,

"Pressurizer Relief Valve Testing," Revision 0, Change 0, incorporated the requirements

and acceptance criteria contained in the applicable design document (i.e., Design

Information Transmittal B-02327, "Stroke Time Acceptance Criteria for

1/2-NRV-152, 153," February 1, 2002). This is considered to be a violation of

10 CFR Part 50, Appendix B, Criterion XI. Because of the very low safety significance,

this violation is being treated as a Non-Cited Violation consistent with Section VI.A of the

NRC Enforcement Policy (NCV 50-316-02-02-02(DRP)). This violation is in the

licensee's corrective action program as CR 02046050.

1R23 Temporary Plant Modifications (71111.23)

a. Inspection Scope

The inspectors reviewed the temporary modification listed below to verify that the

installation was consistent with design modification documents and that the modification

did not adversely impact system operability or availability:

C 2-TM-00-54-R1 Installation of Noise Filtering Resistors on Cables

2-4450PB-2 for 2-ILA-111 and 2-5658PB-2 for 2-ILA-121

The temporary modification installed a 1000 ohm resistor between the shield and

ground on each cable to alleviate unstable indication and spurious alarms for two

SI system accumulator level channels. The inspectors verified that configuration control

of the modification was correct by reviewing design modification documents and

confirmed that appropriate post-installation testing was accomplished. The inspectors

reviewed the design modification documents and the 10 CFR 50.59 evaluation against

the applicable portions of the UFSAR.

b. Findings

No findings of significance were identified.

19

2. RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

.1 Plant Walkdowns and Radiological Boundary Verification

a. Inspection Scope

The inspector conducted walkdowns of selected radiologically controlled areas to verify

the adequacy of radiological boundaries and postings. The inspector reviewed the

administrative controls for access to radiologically significant areas, as specified in

radiation protection (RP) procedures and in radiation work permits (RWPs), and the

physical controls established over those areas walked-down were assessed through

direct observation. Specifically, the inspector walked-down several radiologically

significant work area boundaries (high and locked high radiation areas) in the Unit 1 and

Unit 2 Auxiliary Building and in the Unit 2 Containment Building and performed

confirmatory radiation measurements in the Auxiliary Building to verify that these areas

and selected radiation areas were properly posted and controlled in accordance with

10 CFR Part 20 and the licensees TS.

b. Findings

No findings of significance were identified.

2OS2 As-Low-As-Is-Reasonably-Achievable (ALARA) Planning and Controls (71121.02)

.1 Radiation Dose Goals and Trending

a. Inspection Scope

The inspector reviewed the stations historical outage exposure data for the last several

refueling outages to establish its prior performance relative to the industry. Job specific

and cumulative exposure performance and exposure trends for the first 20-days of the

approximate 40-day Unit 2 refueling outage (U2C13) were reviewed to assess the

licensees current dose performance compared to pre-outage exposure projections.

The inspector also reviewed the licensees dose forecasting practices for those

radiologically significant jobs that were being performed during the outage to determine

if adequate technical bases for outage dose estimates existed. Dose forecasting

practices were also reviewed to determine if outage experiences, craft work group

defined job scope, resource estimates, and industry operating experiences were used to

establish reasonable estimates. Additionally, the inspector reviewed the effectiveness of

the RP organizations exposure tracking for the outage to verify that the licensee could

identify problems with its exposure performance and take actions to address identified

deficiencies.

20

b. Findings

No findings of significance were identified.

.2 Radiological Work Planning

a. Inspection Scope

The inspector reviewed the licensees procedures for ALARA planning and evaluated

several U2C13 ALARA plans to verify consistency with the procedure and to assess

their overall adequacy relative to both current licensee practices and industry standards.

Specifically, the inspector selected the following outage jobs that were projected to

accrue cumulative doses in excess of 3.5 rem and assessed the adequacy of the

radiological controls and the work planning for each:

C Temporary Shielding

C Insulation Activities in Containment

C Scaffold Erection/Removal in Containment

C Steam Generator Manway & Diaphragm Activities

C Steam Generator Primary Work and Platform Activities

C Control Rod Drive Mechanism Inspections

C Reactor Head Control Rod Drive Mechanism Penetration Weld Inspections

C Modify/Replace Pressurizer Spray Line Temperature Sensors

The inspector reviewed the RWP and the ALARA plan developed for each job and

assessed the radiological engineering controls and other dose mitigation information

specified in these documents to verify that plans included appropriate controls to reduce

dose. These documents were also reviewed to determine if job history files, licensee

lessons learned, and industry operating experiences were adequately integrated into

each work package. The inspector discussed ALARA planning with several RP staff to

verify that adequate interface existed between contractors, station work groups, and the

ALARA staff during job planning. Additionally, plans to improve ALARA planning

through more detailed task analysis were discussed with RP management and ALARA

staff.

a. Findings

No findings of significance were identified.

.3 Implementation of ALARA Controls and Radiological Oversight of Work

a. Inspection Scope

The inspector selected the following high exposure or high radiation area jobs

conducted during the outage and reviewed the execution of the ALARA program:

C Install, Modify and Remove Scaffolds in Containment (RWP # 022136)

C Shielding Activities in Containment (RWP # 022119)

C Modify/Replace Pressurizer Spray Line Temperature Sensor (RWP # 022170)

21

The inspector discussed job performance with involved RP staff, and total effective dose

equivalent (TEDE) ALARA evaluations completed for these and a variety of other

outage work activities, including steam generator work, were assessed for technical

adequacy. Work in progress reports and radiological survey data for these and other

selected jobs, as applicable, were also reviewed to assess their adequacy and

consistency with licensee procedures. The pre-job brief for a transfer canal dive to

repair a valve was attended to verify that the work activity was adequately planned and

that radiological control information was exchanged effectively. The inspector evaluated

the licensees radiological engineering controls utilized at selected work locations to

determine if the controls were consistent with those specified in the ALARA plans. The

inspector also observed and questioned both RP staff that provided job coverage for

various outage activities and radiation workers (radworkers) involved in outage work to

verify that they had adequate knowledge of radiological work conditions and ALARA

controls. Additionally, the inspector reviewed measurements and calculations

completed by the RP staff to assess worker dose from skin contaminations and intakes

to determine if the methodology was technically sound and if the results were accurate.

b. Findings

No findings of significance were identified.

.4 Verification of Exposure Estimates and Exposure Tracking Systems

a. Inspection Scope

The inspector reviewed the methods and assumptions used by the ALARA group to

develop U2C13 dose estimates and compared collective outage and individual job dose

performance and trends during the first 2 weeks of the outage to assess dose

performance and to determine the accuracy of pre-outage projections. The inspector

reviewed job dose history files, dose reductions anticipated through ALARA initiatives,

and task specific breakdown analyses employed for certain jobs to verify that they were

appropriately used to forecast outage doses. In particular, the inspector reviewed

containment scaffolding work, which was anticipated to expend greater than 25 rem of

exposure and to exceed original dose projections by more than 50 percent, and

discussed its dose performance with ALARA staff. The review was conducted to

determine whether the licensee had identified those factors that contributed to additional

dose and/or inaccurate dose estimates. The inspector also reviewed the licensees

process used to revise dose estimates and capture lessons learned to verify compliance

with the licensees ALARA procedure. As of February 7, 2002, the licensee had

recorded a collective outage exposure of approximately 105 rem, compared to its

original estimate of about 95 rem for that stage of the outage. Selected work in

progress reports were examined to evaluate the licensees ability to assess the

effectiveness of a job, to execute its ALARA plan, and to institute changes in work plans,

if warranted. The licensees exposure tracking system was also reviewed to determine if

the level of exposure tracking detail, exposure report timeliness, and report distribution

were sufficient to support the control of outage exposures.

22

b. Findings

No findings of significance were identified.

.5 Source Term Reduction and Control

a. Inspection Scope

The inspector reviewed the licensees source term reduction activities, focusing on

recent initiatives including those taken for the outage such as flushing, installation of

shielding and changes in plant operations during the Unit 2 cool-down process. The

inspector also evaluated the licensees water chemistry control program implemented

during the Unit 2 shutdown and its impact on source term reduction to determine

whether the program was implemented consistent with station procedure and industry

practices. First time water chemistry initiatives, which included a revised de-lithiation

initiative to achieve acidic conditions earlier during cool-down and a revised RCS degas

process to maintain corrosion products in soluble form, were reviewed by the inspector.

These initiatives were reviewed to verify that the licensee implemented adequate

practices for corrosion and source term control. The licensees overall source term

reduction program was assessed to verify that other initiatives such as cobalt reduction

through stellite control were being pursued and to determine if a viable, progressive

source term control program was in place.

b. Findings

No findings of significance were identified.

.6 Identification and Resolution of Problems

a. Inspection Scope

The inspector reviewed the results of an RP self-assessment completed as part of an

ALARA outage planning readiness review and CRs generated by the RP staff during the

outage to evaluate the effectiveness of the RP organizations ability to identify and

correct problems. The inspector also reviewed outage related Performance Assurance

Department field observations, RP program related CRs generated by other station

departments, and investigation reports related to outage RP issues to verify that the

licensee adequately identified individual problems and trends, determined contributing

causes and extent of condition, and developed appropriate corrective actions.

a. Findings

On January 28, 2002, the licensee identified that a contract worker failed to stop work

and leave the radiologically controlled area (RCA) as instructed by a radiation protection

technician (RPT). The worker was instructed to leave the area because the individuals

dose approached the RWP administrative limit established at 200 mrem for the day.

The worker was conducting accumulator check valve testing in the Unit 2 lower

containment. The test utilized an acoustic monitoring device, and the individual was an

expert in setup and data results analysis. The RPT initially instructed the individual to

23

leave containment just prior to the start of the data acquisition portion of the test. When

the worker did not comply with the instruction, the RPT informed an RP supervisor of the

problem, returned to the job site minutes later and heard the workers electronic

dosimetry (ED) accumulated dose alarm. The RPT then instructed the worker to leave

the area a second time. The worker again failed to comply with the RPTs instructions,

but shortly thereafter completed the data acquisition portion of the test, confirmed that

good data was obtained, and then vacated the area.

After learning of the incident, radiation protection supervision immediately suspended

the workers access to the RCA and documented the occurrence in CR 02029016. The

worker was counseled and coached by the licensee and allowed to return to work about

an hour later to complete the testing. After the work was complete, the individual did not

reenter the RCA. The licensee investigated the incident and on January 29, 2002,

released the individual from the site because the licensee concluded that the individual

chose not to comply with RP procedures. According to the licensees preliminary

investigation, the worker failed to obey the RPTs instructions because the individual:

(1) spent considerable time setting-up the test equipment and was about to start the

test; (2) anticipated completing the data acquisition portion of the test in a short time

without significant additional dose; and (3) was an expert in the testing operation which

involved "critical path" work that the worker felt pressure to complete without further

delay. According to the licensees preliminary investigation, the individual was aware of

the requirement to comply with RP instructions and to immediately leave the work area

upon receiving an ED alarm but decided not to comply for the reasons specified above.

On January 31, 2002, the D. C. Cook station newspaper included an article that

summarized the incident and reminded workers to follow RP procedures.

The dose received by the worker for the day was 201 mrem, just above the 200 mrem

administrative dose limit established on the RWP that governed the check valve test

work. The inspector reviewed area survey information to assess the radiological safety

significance of the incident and determined that a potential for an overexposure did not

exist had the worker continued to remain in the area longer. Work area radiation levels

ranged from about 20 to 250 mrem/hour, depending on the workers location relative to

the valve being tested. At the time of the incident, the worker was positioned near the

test equipment which was set-up in a lower radiation field. The worker accumulated a

dose of about 3 mrem from the time he was initially instructed by the RPT to leave the

area and several minutes later when he complied. Based on inspector discussions with

members of the RP staff and review of the licensees preliminary investigation, the

inspector concluded that the workers actions appeared to be in violation of

RP procedure PMP-6010-RPP-001, "General Radiation Worker Instructions." This

incident is considered to be an URI pending further NRC review to determine potential

enforcement actions (URI 50-316-02-02-03(DRS)).

24

4. OTHER ACTIVITIES (OA)

4OA1 Performance Indicator Verification (71151)

.1 Unit 2 Turbine Driven Auxiliary Feedwater Pump (TDAFWP) Fault Exposure

(Closed) URI 50-316-01-19-03: "Apparent Violation of 10 CFR 50, Appendix B,

Criterion V for the Failure to Incorporate Adequate Quantitative Acceptance Criteria in

TDAFWP Maintenance Instructions."

a. Inspection Scope

On August 10, 2001, the Unit 2 TDAFWP failed to start during three successive start

attempts. The inspectors documented a preliminary evaluation of this issue in NRC

Inspection Report 50-315/316-01-019(DRP), Section 4OA1.1. To support additional risk

evaluation of the TDAFWP failure in accordance with the SDP, the inspectors identified

this issue as URI 50-316-01-19-03. Prior to the completion of the NRC staffs risk

significance evaluation for this issue, an additional failure of the Unit 2 TDAFWP

occurred on January 18, 2002. The inspectors reviewed the circumstances of this

subsequent TDAFWP failure to fully assess the adequacy of the licensees previous

apparent cause evaluation and to evaluate the risk significance of the repetitive failure.

b. Findings

The inspectors identified an Apparent Violation of low to moderate risk significance

(White) associated with failure of the licensee to take appropriate corrective actions to

prevent a repetitive failure of the Unit 2 TDAFWP.

Description

On January 18, 2002, the Unit 2 TDAFWP failed to start during performance of time

response testing. The licensee determined that the failure was due to the unlatching of

the TDAFWP trip throttle valve (2-QT-506). A similar TDAFWP failure occurred on

August 10, 2001. Following the January 18, 2002 failure, the licensee declared the

TDAFWP inoperable but reset the trip latch mechanism to align the TDAFWP for

auto-start capability. Although no corrective maintenance was performed on the

TDAFWP, the pump started satisfactorily on January 19, 2002 following a pre-planned

reactor trip to support the Cycle 13 refueling outage.

Following the January 18, 2002 TDAFWP failure, the licensee initiated CR 02018064

and performed a root cause evaluation to determine the cause of the repetitive pump

failures. The licensee concluded that incorrect machining of the trip throttle valve trip

hook, resulting in inadequate alignment of the trip hook and latching up lever faces, was

the root cause of the repetitive failure. In order to open the trip throttle valve, the trip

hook engages the latching up lever to permit admission of steam to the turbine. During

a turbine trip, the trip hook would rotate on the trip hook pin and release the latching up

lever to close the trip throttle valve. Incorrect machining of the trip hook resulted in a

rotational force on the trip hook that would cause the latching mechanism to disengage.

25

A contributing cause to the pump failure was an the incorrect alignment specification for

engagement between the trip hook and latching up lever previously discussed in NRC

Inspection Report 50-315/316-01-19(DRP). Proper machining of the trip hook would

result in a parallel alignment of the trip hook face and the latching up lever face (this

would allow adequate surface area engagement to prevent inadvertent unlatching of the

trip throttle valve).

Following the January 18, 2002 pump failure, the licensee performed a visual inspection

of the trip throttle valve and determined that the faces of the trip hook and latching up

lever were not in parallel alignment, a condition which would cause the trip hook to

disengage the latching up lever under load. The licensee determined that the latch face

of the trip hook had been machined at an incorrect angle, resulting in the failure to

obtain parallel alignment between the faces of trip hook and latching up lever. The result

of this defect was that the trip hook and latching up lever did not engage with full latch

face surface contact, but instead engaged along a line at the edge of the latching up

lever. The defective trip hook mechanism was originally purchased from the Terry

Steam Turbine Company in 1985 under the vendors quality assurance program. The

trip hook was installed on the Unit 2 TDAFWP following a pump failure in June 14, 2000.

The licensee determined that, because the critical dimensions and characteristics of the

trip hook mechanism were not provided to D.C. Cook, it was previously unable to

identify the condition. Because the trip hook and latching up lever engaged along a line

at the end of the latching up lever rather than full surface area contact (due to the

incorrect trip hook latch face angle), it would not have been possible to obtain a

75 percent surface contact during an alignment blue check. Consequently, the licensee

determined that use of the incorrect blue check contact alignment acceptance criteria in

trip throttle valve maintenance procedure 12-MHP 5021.056.007 (i.e., 75 percent line

contact vice 75 percent surface area contact) may have delayed identification of this

condition. Specifically, with the incorrect contact angle between the trip hook and

latching up lever, a 75 percent surface area blue check contact alignment acceptance

criteria would not have been attainable and the installation of the defective trip hook

could have been discovered in June 2000. The Unit 2 TDAFWP was repaired and

retested satisfactorily on February 24, 2002. After the second failure of the Unit 2

TDAFWP, the licensee performed a visual inspection of the Unit 1 TDAFWP and

determined that the contact angle between the trip hook and latching up lever appeared

acceptable. The inspectors concluded that the licensees root cause evaluation was

thorough and reasonable.

Because of the repetitive TDAFWP failures, the inspectors reviewed the effectiveness of

the licensees corrective actions for the August 10, 2001 TDAFWP failure. The

inspectors determined that the licensees failure to promptly evaluate information

obtained during the investigation of the August 2001 TDAFWP failure contributed to the

January 2002 pump failure. On December 13, 2001, the licensee received information

from the trip throttle valve vendor regarding the required specifications for alignment

between the trip hook and the latching up lever. Specifically, the vendor identified the

necessary geometry of the trip hook to avoid generation of a force that would tend to

unlatch the trip mechanism. Additionally, the vendor clarified that the 75 percent blue

check acceptance criteria for alignment between the trip hook and latching up lever

referred to a surface area contact rather than a line criteria. Because the correct blue

check contact alignment criteria (i.e., line contact vice area contact) was not known to

26

the licensee immediately following the August 10, 2001 TDAFWP failure, the licensee

had previously aligned the trip mechanism using a 75 percent line contact acceptance

criteria in August 2001. On December 20, 2002, the licensee performed an operability

evaluation under CR 01354104 to evaluate the use of the line contact trip throttle

mechanism engagement criteria and concluded that both the Unit 1 and Unit 2

TDAFWPs were operable based, in part, on previous successful testing of the pumps.

Although the licensee planned to perform maintenance on the Unit 2 TDAFWP trip

throttle valve during the Cycle 13 refueling outage, no corrective maintenance was

performed on the Unit 2 TDAFWP to evaluate and correct these potential failure

mechanisms prior to the January 18, 2002 failure. Subsequent evaluation by the

licensee following the January 18, 2002 failure identified that the 75 percent area blue

check contact alignment was not met and that the trip hook did not conform to the

required geometric specifications. The inspectors concluded that timely corrective

actions to verify trip hook alignment and geometry consistent with vendor

recommendations could have prevented the January 18, 2002 pump failure.

Based on this corrective action weakness, the inspectors concluded that the licensee

failed to take timely and appropriate corrective action to prevent a repetitive failure of the

Unit 2 TDAFWP. As discussed in NRC Inspection Report 50-315/316-01-19(DRP), the

inspectors previously determined that the licensee failed to specify the correct trip

throttle valve alignment criteria in maintenance procedure 12-MHP 5021.056.007,

"Turbine Driven Auxiliary Feed Pump Trip and Throttle Valve Linkage Adjustment,"

Revision 2. The inspectors concluded that the circumstances and issues associated

with the failure to implement appropriate acceptance criteria in 12-MHP 5021.056.007

were closely related to these corrective action weaknesses. Because the failure to take

timely corrective action for known deficiencies associated with the trip throttle valve

alignment criteria resulted in a repetitive failure of the Unit 2 TDAFWP, the inspectors

considered the corrective action weaknesses to be a more significant regulatory

concern. Consequently, the inspectors evaluated the identified licensee performance

deficiencies, including procedure and corrective action weaknesses, as a single problem

resolution issue.

Analysis

The inspectors assessed this issue using the SDP. The inspectors concluded that the

failures of the Unit 2 TDAFWP and associated fault exposure unavailability time had a

credible impact on safety and was therefore more than a minor concern. Specifically,

the TDAFWP provides secondary decay heat removal capability during certain accidents

including transients, loss of electrical power events, and some losses of primary coolant

events. Consequently, the repetitive failures of the Unit 2 TDAFWP resulting in the

unavailability of a train of auxiliary feedwater was associated with the mitigating systems

cornerstone. The inspectors performed an SDP Phase 1 assessment and determined

that the fault exposure time represented an actual loss of safety function for a single

train of auxiliary feedwater for greater than its TS allowed outage time. As discussed

below, the inspectors estimated that the August 2001 and January 2002 TDAFWP

failures represented approximately 80 days of fault exposure unavailability.

Consequently, the fault exposure time exceeded the TS 3.7.1.2 allowed outage time of

72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> for a single train of auxiliary feedwater. Based on the results from the Phase 1

27

SDP assessment, the inspectors determined that a Phase 2 SDP assessment was

required.

Because of concerns regarding the accuracy of the D. C. Cook Phase 2 worksheets,

especially with respect to crediting the motor driven auxiliary feedwater pump cross-tie

capability from the other unit, it was determined that it would be more appropriate to

perform a Phase 3 SDP assessment using insights from the licensees updated PRA

model. In coordination with the Region III SRA, the following factors were considered

for this risk evaluation:

C Because the inspectors were unable to determine the exact time that the

TDAFWP became incapable of fully performing its safety function during each of

the two fault exposure periods, the inspectors used the "T/2" fault exposure

methodology (i.e., one half the time between the pump failure and the previous

demonstrated successful operation) to assess this issue. Several factors could

degrade the ability of the trip throttle valve to remain engaged during the fault

exposure period and result in the inability to determine an exact failure time,

including: mechanism wear due to ambient vibration, latch face surface

condition, and trip latch mechanism friction. Use of the "T/2"methodology was

also consistent with the guidance provided in the response to Frequently Asked

Question 291 documented in NEI 99-02, "Regulatory Assessment Performance

Indicator Guideline," Revision 2.

C The inspectors did not consider the ability to recover the TDAFWP following an

unsuccessful start attempt. This conclusion was based on the inability of the

licensee to achieve a successful TDAFWP start during three successive start

attempts on August 10, 2001 and the nature of the repair activities required to

restore the pump to an available status. The inspectors noted that the

successful auto-start of the Unit 2 TDAFWP pump following the

January 18, 2002 failure indicated that the TDAFWP could have potentially been

recovered following this failure. However, due to the similarity of the root cause

for the August 2001 and January 2002 pump failures, the inspectors determined

that recovery credit was not warranted.

C Because the August 2001 and January 2002 TDAFWP pump failures shared a

common root cause, the inspectors concluded that the fault exposure associated

with these failures should be combined to appropriately characterize the risk

significance of the issue. The inspectors determined that the last successful

TDAFWP start attempt prior to the January 18, 2002 failure occurred on

November 2, 2001. Therefore, the January 18, 2002 failure represented an

additional 38 days of "T/2" fault exposure for the Unit 2 TDAFWP. Combining

this fault exposure with the previous 42 days of "T/2" fault exposure from the

August 10, 2001 failure resulted in a total "T/2" fault exposure of approximately

80 days. Based on six successful TDAFWP quarterly surveillance test starts

between June 2000 and January 2002 (including a successful surveillance test

between the August 2001 and January 2002 failures), the application of a single,

longer, fault exposure period for this issue was not considered to be reasonable.

28

C Based on the licensees PRA, the TDAFWP had a risk achievement worth value

of 1.41 and the plant had a baseline core damage frequency (CDF) of 4.85E-5

per reactor year.

Using the methodology and assumptions stated above, the SRA determined that

80 days of fault exposure unavailability resulted in an increase in CDF due to internal

events to be approximately 4.4E-6 with a very small risk impact due to external initiating

events.

Evaluating the impact of this issue on the large early release frequency (LERF), the

SRA focused on dual station blackout transients where hydrogen ignitors would not be

available. (The ignitors are designed to burn hydrogen at low concentrations and thus

reduce the potential for large detonations that could challenge containment integrity.)

The SRA reviewed the licensees Level 2 evaluation, which provided a more refined tool

than IMC 0609, Appendix H, "Containment Integrity Significance Determination

Process." Review of the licensees cutsets determined that the contribution of the dual

unit station blackout was small and the probability of such an event was very low. The

final review determined that the change in LERF was approximately 6E-7.

Based on all the contributing factors, the analyst concluded that the risk significance of

the inspection finding due to the change in CDF due to internal, external and LERF

considerations to be of low to moderate risk significance (White).

Enforcement

10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," states, in part, that measures

shall be established to assure that conditions adverse to quality, such as failures,

malfunctions, deficiencies, deviations, defective material and equipment, and

nonconformances are promptly identified and corrected. In the case of significant

conditions adverse to quality, the measures shall assure that the cause of the condition

is determined and corrective action taken to preclude repetition. Contrary to the above,

the licensee failed to take corrective action to prevent repetition of the failure of the

Unit 2 TDAFWP, a significant condition adverse to quality. Specifically, the Unit 2

TDAFWP failed to start on August 10, 2001 due to the failure of the trip throttle valve

latch mechanism to remain engaged during pump start. On December 13, 2001, the

licensee obtained information from the trip throttle valve vendor identifying critical

parameters for the trip hook mechanism geometry and alignment. The licensee failed to

promptly perform corrective actions to verify that the Unit 2 TDAFWP trip hook

conformed to these critical parameters. Consequently, a second failure of the Unit 2

TDAFWP occurred on January 18, 2002 due to the failure of the trip throttle valve latch

mechanism to remain engaged during pump start. Subsequent investigation determined

that the cause of the August 10, 2001 and January 18, 2002 failures was due to

incorrect trip hook geometry and alignment. This issue was determined to be of low to

moderate risk significance (White) after a Phase 3 SDP review. Consequently, this

issue is identified as Apparent Violation (AV 50-316-02-02-04(DRP)) and is in the

licensees corrective action program as CR 02018064. URI 50-316-01-19-03 is closed.

29

4OA3 Event Followup

.1 (Closed) Licensee Event Report (LER) 50-316-2000-012-01: "Failure to Perform

Increased Frequency Surveillance on 2 East Containment Spray Pump," Supplement 1.

The inspectors reviewed the original LER and determined that the licensees failure to

perform increased frequency surveillance testing on the containment spray pump as

required by TS 4.0.5 was a minor issue. The licensee submitted Supplement 1 to

LER 50-316-2000-012 to revise the root cause evaluation for the event. The inspectors

determined that the information provided in Supplement 1 to LER 50-316-2000-012 did

not raise any new issues or change the conclusions of the initial review, which were

documented in NRC Inspection Report 50-315/316-00-20(DRP). This LER is closed.

.2 (Closed) LER 50-315-2001-002-00: "Power Range Nuclear Instrumentation Calibration

Procedure Not in Conformance with TS". On June 22, 2001, the power range nuclear

instrumentation (PRNI) channel functional test for the Unit 1 quarterly calibration was

not conducted in accordance with TS 3.3.1.1, Table 3.3-1, Action 2a. This TS requires

placing the inoperable PRNI channel in the tripped condition within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. To meet the

TS requirement, the PRNI channel is placed in trip before the detectors are

disconnected. Contrary to the TS , the calibration procedure for the PRNI directed that

the bistables for the PRNIs be returned to an untripped state while the detectors are still

disconnected and after the channel has been inoperable for greater than 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. On

August 8, 2001, the licensee received NRC approval of a license amendment to revise

TS 3.3.1.1, Table 3.3-1, Action 2a to increase the amount of time allowed to place an

inoperable PRNI channel in the tripped condition from 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> to 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. On

August 9, 2001, the licensee revised the functional test and calibration procedures to

implement this TS change. The inspectors reviewed the LER and the licensees

corrective actions and did not identify any significant findings. Although this issue was

corrected, it constitutes a violation of minor significance that is not subject to

enforcement action in accordance with Section IV of the NRCs Enforcement Policy.

The licensee entered this violation into its corrective action program as CR 01192045.

This LER is closed.

4OA6 Meetings

.1 Interim Exits

The results of the Occupational Radiation Safety - Access Controls for Radiologically

Significant Areas and ALARA Planning Inspection were presented to Mr. J. Pollock and

other members of licensee management at the conclusion of the inspection on

February 8, 2002. The licensee acknowledged the findings presented. The inspector

asked the licensee whether any materials examined during the inspection should be

considered proprietary. No proprietary information was identified.

The results of the Licensed Operator Requalification Program Inspection were

presented to Mr. B. Wallace and other members of licensee management at the

conclusion of the inspection on March 29, 2002. The licensee acknowledged the

findings presented. The inspectors asked the licensee whether any materials examined

during the inspection should be considered proprietary. No proprietary information was

identified.

30

.2 Resident Inspectors Exit

The inspectors presented the inspection results to Mr. C. Bakken and other members of

licensee management at the conclusion of the inspection on April 5, 2002. The licensee

acknowledged the findings presented. The inspectors asked the licensee whether any

materials examined during the inspection should be considered proprietary. Proprietary

information was examined during this inspection but is not specifically discussed in this

report.

31

KEY POINTS OF CONTACT

Licensee

G. Arent, Manger, Regulatory Affairs

C. Bakken, Senior Vice President, Nuclear Generation

R. Brown, Manager, Operations Training

L. Dean, ALARA Supervisor

S. Freeman, Administrative Assistant, Training Department

R. Gaston, Regulatory Compliance Manager

J. Gebbie, Manager, System Engineering

S. Greenlee, Director, Nuclear Technical Services

N. Jackiw, Regulatory Affairs

E. Larson, Director, Operations

J. Mathis, Regulatory Affairs

R. Meister, Regulatory Affairs

D. Moul, Assistant Manager, Operations

W. Nichols, Supervisor, Operator Requalification Training

D. Noble, Manager, Radiation Protection

T. Noonan, Director, Performance Assurance

J. Pollock, Site Vice President

B. Robinson, General Supervisor, Radiation Protection Support

R. Smith, Assistant Director, Plant Engineering

B. Wallace, Manager, Training

D. Wood, Manager, RadChem Environmental

T. Woods, Regulatory Affairs

NRC

A. Vegel, Chief, Reactor Projects Branch 6

S. Burgess, Senior Reactor Analyst

H. González, Nuclear Safety Intern

D. Rivera-Martinez, Nuclear Safety Intern

32

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-316-02-02-01 URI Failure to perform adequate maintenance and testing on

valve 2-CS-369 resulted in gas binding the Unit 2 west

centrifugal charging pump (Section 1R19)

50-316-02-02-02 NCV Failure to use valid acceptance criteria for stroke time testing

the Unit 2 pressurizer power operated relief valves

(Section 1R22)

50-316-02-02-03 URI Contract worker failed to comply with radiological protection

instructions and to immediately vacate a work area upon

receiving an electronic dosimeter alarm (Section 2OS2.6)

50-316-02-02-04 AV Failure to take prompt corrective action to prevent repetitive

failure of the Unit 2 turbine driven auxiliary feedwater pump

(Section 4OA1)

Closed

50-316-02-02-02 NCV Failure to use valid acceptance criteria for stroke time testing

the Unit 2 pressurizer power operated relief valves

(Section 1R22)

50-316-01-19-03 URI Apparent violation of 10 CFR Appendix B, Criterion V for the

failure to incorporate adequate quantitative acceptance

criteria in turbine driven auxiliary feedwater pump

maintenance instructions (Section 4OA1)

50-316-2000-012-01 LER Failure to perform increased frequency surveillance on 2 east

containment spray pump (Section 4OA3)

50-315-2001-002-00 LER Power range nuclear instrumentation calibration procedure

not in conformance with technical specifications

(Section 4OA3)

Discussed

50-316-2000-012-00 LER Failure to perform increased frequency surveillance on 2 east

containment spray pump (Section 4OA3)

33

LIST OF ACRONYMS USED

ADAMS Agency-wide Documents and Management System

AEP American Electric Power

AFW Auxiliary Feedwater

ALARA As Low As Is Reasonably Achievable

ATR Administrative Technical Requirement

AV Apparent Violation

CCP Centrifugal Charging Pump

CCW Component Cooling Water

CDF Core Damage Frequency

CFR Code of Federal Regulations

CR Condition Report

CRDM Control Rod Drive Mechanism

DC Direct Current

DCP Design Change Package

DIT Design Information Transmittal

DRP Division of Reactor Projects

DRS Division of Reactor Safety

ECCS Emergency Core Cooling System

ED Electronic Dosimeter

EHP Engineering Head Procedure

ESW Essential Service Water

gpm or GPM Gallons Per Minute

IHP Instrumentation Head Procedure

IMC Inspection Manual Chapter

JO Job Order

JPM Job Performance Measure

KV Kilo-volt

LER Licensee Event Report

LERF Large Early Release Frequency

LOR Licensed Operator Requalification

LORT Licensed Operator Requalification Training

LTOP Low Temperature Over-pressure Protection

MHP Maintenance Head Procedure

NCV Non-Cited Violation

NRC Nuclear Regulatory Commission

NUMARC Nuclear Management and Resources Council

OA Other Activities

OHP Operations Head Procedure

ORAM Outage Risk Assessment and Management

OSHA Occupational Safety and Health Administration

PARS Publically Available Records

PMI Plant Managers Instruction

PMP Plant Managers Procedure

PORV Power Operated Relief Valve

PRA Probabilistic Risk Assessment

PRNI Power Range Nuclear Instrument

Radworker Radiation Worker

34

RCA Radiological Controlled Area

RCS Reactor Coolant System

RO Reactor Operator

RP Radiation Protection

RPT Radiation Protection Technician

RWP Radiation Work Permit

RWST Refueling Water Storage Tank

SDP Significance Determination Process

SI Safety Injection

SOER Significant Operating Event Report

SRA Senior Reactor Analyst

SRO Senior Reactor Operator

SSC Structures, Systems, and Components

STP Surveillance Test Procedure

TBD To Be Determined

TDAFWP Turbine Driven Auxiliary Feedwater Pump

TDB Technical Data Book

TEDE Total Effective Dose Equivalent

TS Technical Specification

U2C13 D.C. Cook Unit-2, 13th Refueling Outage

UFSAR Updated Final Safety Analysis Report

URI Unresolved Item

VCT Volume Control Tank

35

LIST OF DOCUMENTS REVIEWED

1R04 Equipment Alignment

Plant Managers Restraint of Transient Material Revision 1

Procedure (PMP)

5020.RTM.001

12-MHP-5021.SCF.001 Scaffolding Guidelines Revision 0b

01-OHP-5030.001.001 Operations Plant Tours Revision 19b

01-OHP-4021.016.003 Operation of the Component Cooling Revision 15a

Water System During System Startup and

Power Operation

Flow Diagram CCW [Component Cooling Water] Pumps Revision 40

OP-1-5135-40 and CCW Heat Exchangers

Flow Diagram CCW Safety Related Loads Revision 41

OP-1-5135A-41

Flow Diagram CCW Miscellaneous Services Auxiliary Revision 3

OP-1-5135C-3 Building

Flow Diagram Auxiliary Feedwater Unit 1 Revision 50

OP-1-5106A-50

Condition Report (CR) NRC Identified That Procedure March 8, 2002

02067020 01-OHP-4023-SUP-002, "Restoration of

Reserve Power to 4KV [Kilovolt] Buses"

Needs to Be Revised to Correct

Typographical Error

CR 02084028 1-CFA-421 (West CCP [Centrifugal March 24, 2002

Charging Pump] Coolers CCW Outlet Low

Flow Alarm Switch) Indicates High

Off-scale and Greater Than Limit of 80

Gallons Per Minute (GPM) Specified in

01-OHP-5030-001-001

CR 02085001 NRC Identified Several Scaffolding March 25, 2002

Installations That Were Contacting Safety

Related Equipment

CR 02089018 NRC Identified Packing Leak on March 30, 2002

1-CCW-404W

CR 02089019 NRC Identified Conduit From 1-CMO-420 March 30, 2002

Has Pulled Out of the Junction Box

36

CR 02089020 NRC Identified Packing Leak on March 30, 2002

1-CCW-187W

CR 02089023 NRC Identified Packing Leak on March 30, 2002

1-CCW-197S

1R05 Fire Protection

Updated Final Safety Fire Protection System

Analysis Report,

Section 9.8.1

D. C. Cook Nuclear Plant Fire Hazards Revision 8

Analysis, Units 1 and 2

D. C. Cook Nuclear Plant Units 1 and 2 February 1995

Probabilistic Risk Assessment, Fire

Analysis Notebook

National Fire Protection Standard for Gaseous Hydrogen at

Association 50A Consumer Sites

Branch Technical Storage of Flammable Gases

Position 9.5-1,

Appendix A,

Section D.2

PMP 2270.CCM.001 Control of Combustible Materials Revision 1

PMP 2270.FIRE.002 Responsibilities for Cook Plant Fire Revision 0

Protection Program Document Updates

PMP 2270.WBG.001 Welding, Burning and Grinding Activities Revision 0

Plant Managers Fire Protection Revision 26

Instruction (PMI) 2270

12-QHP-4030-STP.009 Inspection of Fire Dampers Protecting Revision 0

Safety-Related Areas

12-PPP-4030-066-021 Inspection of Fire Dampers Protecting Revision 1

Safety-Related Areas

Design Change Relocate Main Generator Hydrogen Bulk Revision 0a

Package (DCP) Storage Tanks from the Unit 1 Side to the

12-DCP-5012 Unit 2 Side

Job Order (JO) Perform 18 Month Surveillance of August 20, 1999

R0084548 Administrative Technical Requirements

Fire Dampers

37

JO R0096948 Perform 18 Month Surveillance of April 2, 2001

Administrative Technical Requirements

Fire Dampers

Drawing 12-5717-15 Heating and Ventilating Auxiliary Building Revision 15

Center North, South & West Plan Floor

Elevation 609-0"

CR 99-18790 OSHA [Occupational Safety and Health July 17, 1999

Administration] Requirement Not Being Met

for Reactor Hydrogen System

CR 02053067 NRC Identified That Cable Separation in February 22, 2002

the Unit 1 West CCP Room Did Not

Conform to D. C. Cook Specification

CR 02064061 List of NRC Identified Issues in the March 5, 2002

Switchgear Cable Vault

CR 02064067 NRC Identified Issue, 1-EIC3 Cable Tray March 5, 2002

Missing Screws

CR 02064070 NRC Identified Excessive Combustible March 5, 2002

Trash in the Unit 1 Auxiliary Cable Vault

1R11 Licensed Operator Requalification Program

Licensed Operator Requalification Training

(LORT) Simulator Evaluation Scenarios for

March 6, 2002

LORT Plan D. C. Cook Licensed Operator 2001-2002

Requalification (LOR) 2 Year Training Plan

Written Exam 2002 Licensed Operator Requalification March 14, 2002

RQ2526 A-R, Biennial Written Exam - Crew A

RQ2526 A-S Week Six - Reactor Operator (RO) and

Senior Reactor Operator (SRO)

Operating Exam 2002 Two Simulator Scenarios: March 15, 2002

Simulator Scenarios RQ-E-1712A, RQ-E-2008A

Operating Exam 2002 Five JPMs: RO-O-E235 (Revision 3), Various

Job Performance RO-O-E026 (Revision 7), RO-O-S001

Measures (JPMs) (Revision 3), AE-O-E217 (Revision 10),

AE-O-N001 (Revision 6)

TI-TROP-01 Training Program Examination Revision 8,

Requirements February 22, 2002

38

TAP-400 Systematic Approach to Training Revision 2,

Implementation September 25, 2001

TAP-400-040 Conduct of Training Revision 0,

October 8, 1999

TIF (IMP 03) Weekly Training Attendance Sheets Year 2001

(Year 25 (2001), Crews B, C, D, and

Validation)

TIF (IMP 10) Remediation Qualification Attempt Reports Year 2002

TIF (IMP 27) Simulator Crew Evaluation Standards Revision 5,

February 21, 2002

TIF (IMP 29A) SRO Individual Simulator Performance March 27-29, 2002

Evaluations - Crew A - Week Six

TIF (IMP 29B) RO Individual Simulator Performance March 27-29, 2002

Evaluations - Crew A - Week Six

TIF (IMP 29D) Shift Manager Simulator Evaluations - March 27-29, 2002

Crew A - Week Six

TIF (IMP 29E) JPM Summary Sheets - Crew A March 27-29, 2002

TIF (IMP 47) Missed Scheduled Training Notifications Year 2001-Various

TAP-600-030 Simulator Configuration Control Revision 1,

July 27, 2001

TPD-600-EPT Emergency Plan Training Program Revision 1,

Description December 20, 2001

TPD-600-LOR LORT Program Description Revision 5,

October 31, 2001

LORT Task List Task List Review for LOR Years 26 and 27 2001/2002

(RO/SRO Requal years 2001/2002)

LORT 2 Year Matrix 2 Year Training Cycle (2001/2002) Matrix 2001/2002

Listing Period, Theme, Dominant Accident

Sequence from IPE, Selected Tasks,

Topics, and Procedures

Feedback Forms Ten LOR Crew Training Assessment January 2001

Debrief Completed Forms through

December 2001

OHI-2070 Training and Qualification Revision 14,

June 06, 2001

39

OHI-2070, Operator License/Shift Technical Advisor 1st Quarter 2002

Attachment 8 Status Report

OHP-4025.001.001 Emergency Remote Shutdown Revision 3,

May 15, 2001

PMP 2070.600 Training Administration and Qualification Revision 0,

May 30, 2001

SA-2000-TRN-001 Training Comprehensive Self Assessment September 22, 2000

SA-2001-TRN-009 Training Comprehensive Self Assessment January 11, 2002

PA-01-16 Performance Assurance Audit on Training February 9, 2001

through

March 9, 2001

Computer Listing Classroom Attendance Computer Listing June 2000

for RQ-C-2534 (Technical Specifications through

and Bases for 3/4.1 & 3/4.2), RQ-C-2544 July 2001

(Emergency Diesel Generator), RQ-C-2573

(Emergency Plan Procedures)

Action Time Matrix Operator Action Time Requirements by November 28, 2000

Procedure Based on DIT-B-01061-05

Medical Records Selection of Eight Licensed Operator Various

Medical Records (Four SROs and Four

ROs)

Medical Records Computer Print Out - Periodic Report on Various

License Medical Data (Medical Exam Due

Dates)

Watch Proficiency Log Licensed Operator Proficiency Watch 1st Quarter 2002 -

Record Various

CR P-00-09097 Condition Report Concerning Inconsistent June 23, 2000

Procedure Use

CR 01046023 Condition Report Concerning Repeat February 15, 2001

Failure to Properly Store Training Records

CR 01047027 Condition Report Concerning Apparent February 16, 2001

Cause and Extent of Condition Evaluation

Not Conducted In Accordance With

Requirements

CR 02052065 Discrepancies on Annual LOR Examination February 21, 2002

Material for the First Week of Examinations

40

CR 01054050 Condition Report Concerning Actions February 23, 2001

Taken for Apparent Cause Not

Documented

CR 01057044 Condition Report Concerning Failure to February 26, 2001

Include Cross Reference to Condition

Reports

CR 01067028 Condition Report Concerning Training March 08, 2001

Department Compliance with Procedure

Requirements

CR 02074043 Lack of Validation for a New or Significantly March 13, 2002

Modified Scenarios

CR 02074044 Potential Examination Compromise During March 14, 2002

Written Exam Administration

CR 02087034 Incorrect Emergency Plan Classification March 27, 2002

Number Referenced in a Simulator

Evaluation Scenario - RQ-E-2008A

CR 02088010 Requirement to Notify the NRC of Possible March 29, 2002

10 CFR 55.25 Condition Based on

Medication Prescribed to an Operator

CR 02092037 Adequacy of Completing the Plant Accident April 2, 2002

Notification Forms for Emergency Plan

Notifications in Real Time

CR 02092039 Appropriateness of Scheduling and April 2, 2002

Administering the Biennial Written

Examination During the First Year of the

2-Year Plan

CR 02092042 JPMs Selected During the Annual April 2, 2002

Operating Examination Having Greater

Than 50 Percent Repeatability

CR 02092044 Emergency Remote Shutdown Procedure April 2, 2002

Inconsistencies

1R12 Maintenance Rule Implementation

12-EHP-5035-MRP-001 Maintenance Rule Program Administration Revision 4

NUMARC 93-01 Industry Guideline for Monitoring the Revision 2

Effectiveness of Maintenance at Nuclear

Power Plants

41

Donald C. Cook Probabilistic Risk April 13, 1992

Assessment

Hydrogen Ignitor (DIS) System Notebook

Maintenance Rule Scoping Document for October 11, 2001

the Hydrogen Ignitor System

Maintenance Rule Scoping Document for Revision 1

the Circulating Water System

Maintenance Rule Scoping Document for Revision 1

the Compressed Air System

Maintenance Rule (a)(1) Action Plan No Date

Briefing Sheet for the Unit 1 Circulating

Water System

Maintenance Rule (a)(1) Action Plan for the Revision 0

Unit 1 Circulating Water System August 3, 2001

Maintenance Rule (a)(1) Action Plan for the Revision 1

Unit 1 Circulating Water System March 5, 2002

Maintenance Rule Performance Monitoring February 27, 2000

Data for the Compressed Air System through

February 27, 2002

Maintenance Rule Reliability Failures March 18, 2002

(3/18/00 to 3/18/02) for All Systems Where

Failures Have Exceeded Performance

Criteria By 50 Percent or Greater

EP 01-086 Maintenance Rule Expert Panel Meeting May 17, 2001

Minutes

System Health Report for the Unit 1 October 1, 2001

Circulating Water System through

December 31, 2001

System Health Report for the Unit 2 October 1, 2001

Circulating Water System through

December 31, 2001

System Health Report for the Compressed October 1, 2001

Air System through

December 31, 2001

JO 01079034-01 2-HE-10E Inspect Condenser 24 Inch January 23, 2002

Supply Piping

Work Request 2-HE-10W Inspect Condenser 24 Inch February 9, 2002

01088050 Supply Piping

42

CR 00-8322 Low Voltage and Current on Unit 2 Trains June 7, 2000

A and B Lower Ignitors

CR 00-8410 Voltage Regulator 2-VR-LDISA-2 Voltage June 8, 2000

Cannot Be Adjusted

CR 00-8412 Voltage Regulator 2-VR-LDISB-4 Output June 8, 2000

Voltage Cannot Be Adjusted

CR 00-9307 The Glow Plug for Hydrogen Ignitor June 28, 2000

2-UDISA-A6 Was Replaced but Post

Maintenance Testing Was Not Performed

as Specified in the JO

CR 00-10893 Unit 2 Plant Air Compressor Surged and August 4, 2000

Could Not be Reloaded to Provide Plant

and Control Air

CR 00-11711 Expert Panel Approved (a)(1) Status for the August 23, 2000

Hydrogen Ignitor System Based on

Exceeding the Performance Criteria for

Unavailability

CR 00256041 2-VR-LDISB-4 Output Voltage out of September 12, 2000

Specification High 122.56 Volts (118 - 122

Volts)

CR 00310018 Distributed Ignition Voltage Regulator November 4, 2000

Transformers Are Defective

CR 01012015 The Unit 2 Containment Hydrogen Glow January 12, 2001

Plugs Are Obsolete and must Be Replaced

CR 01046054 A Manual Reactor Trip Was Performed February 15, 2001

Upon Recognition That the East Main

Feedwater Pump Had Tripped on High

Back Pressure

CR 01047054 Lower Containment Train B Voltage February 16, 2001

Regulator-4 (2-LDISB-4) Reading High Out

of Specification at 230 Volts

CR 01061036 Installed Breaker Has Incorrect Size March 2, 2001

Current Transformers

CR 01159049 Re-perform a Maintenance Rule Evaluation June 8, 2001

for the Condition Described in CR 00-8322

CR 01163041 Problem Identified with Maintenance Rule June 12, 2001

Evaluation for CR 00-8321 Involving a

Failure of Glow Plug A6

43

CR 01163043 Discrepancies Identified in Maintenance June 12, 2001

Rule Evaluation for CR 00256041

CR 01171032 CR 00-8412 Maintenance Rule Evaluation June 20, 2001

Is Inadequate

CR 01184053 Hydrogen Ignitor System Maintenance July 3, 2001

Rule Scoping Document Has No "Trigger

Value"

CR 01207075 The Maintenance Rule Evaluation July 26, 2001

Performed Under CR 00-10893 Was

Inadequate

CR 01277005 Review of Previously Completed October 4, 2001

Maintenance Rule Evaluation for

CR 00330032 Indicates the Evaluation May

Be Lacking in Detail, Incorrect, or the

Conclusions Not Fully Supported

CR 01310021 2-VR-LDISB-4 Will Not Maintain November 6, 2001

Acceptable Voltage Value

CR 02080014 NRC Identified That Maintenance Rule March 21,2002

Evaluation of CR 01163041 for a Glow

Plug Failure Incorrectly Concluded That the

Failure Was Not a Functional Failure

CR 02080016 NRC Identified Inconsistency in March 21, 2002

Maintenance Rule Scoping Document for

the Distributed Ignition System Regarding

System PRA Risk Significance

Maintenance Rule Scoping Document Revision 1

Component Cooling Water System

System Health Report Period 10/31/01 to

Component Cooling Water 12/31/2001

CR 00356032 Component Cooling Water Maintenance December 21, 2000

Rule History Review

CR 01186039 Maintenance Rule Evaluation for CR July 5, 2001

00323052 associated with low CCW flow to

a CTS pump was inadequate

CR 01101073 2-CCR-440 failed to indicate closed during April 11, 2001

IST testing

CR 00241011 CCW Surge Tank Level Indicator August 28, 2000

2-CLR-410 failed

44

CR 01268056 Indications Found in Welds for CCW Heat September 25, 2001

Exchanger Divider Plate

CR 01277001 1-CCR-440 Failed IST Stroke Time Testing October 4, 2001

1R13 Maintenance Risk Assessments and Emergent Work Control

PMP-2291-OLR-001 On-Line Risk Management Revision 2

NUMARC 93-01 Industry Guideline for Monitoring the Revision 2

Effectiveness of Maintenance at Nuclear

Power Plants, Section 11, "Assessment of

Risk Resulting From Performance of

Maintenance Activities"

PMP 2291-OLR-001 On-Line Risk Management Work Schedule March 10-16, 2002

Data Sheet 1 Review and Approval Form

Cycle 40, Week 9

PMP 2291.OLR.001 On-Line Risk Management Work Schedule March 24 - 30, 2002

Data Sheet 1 Review and Approval Form

Cycle 40, Week 11

Unit 2 Control Room Logs March 23-24, 2002

Unit 1 and 2 Supervisors Turnover Logs March 14, 2002

Clearance Log, Units 1 and 2 March 14, 2002

JO R0214681 2-PP-10W, Change Oil in Bearing August 16, 2001

Reservoir

JO R0220047 2-PP-10W, Change Oil in Bearing March 24, 2002

Reservoir

CR 02075007 NRC Identified Several Issues Involving March 14, 2002

Housekeeping, Scaffolding, and Restraint

of Transient Material

CR 02082003 Failure of Main Turbine Control Valves March 23, 2002

During Testing

CR 02082006 Unit 2 Control Rods Withdrew Continuously March 23, 2002

Without Temperature Error Mismatch

CR 02098031 NRC Identified That Post Maintenance April 8, 2002

Testing for the 2 West CCW Pump on

March 24, 2002 Was Not Performed In

Accordance With the Associated Job Order

45

1R15 Operability Evaluations

D.C. Cook Nuclear Plant Unit 2 Technical

Specifications

D. C. Cook Nuclear Plant Updated Final

Safety Analysis Report

NRC Safety Evaluation Report for Cook September 1, 1995

Nuclear Plant Unit 2 Amendment 185

Generic Letter 91-18 Information to Licensees Regarding NRC Revision 1

Inspection Manual Section on Resolution of

Degraded and Nonconforming Conditions

PMP-7030-ORP-001 Operability Determinations Revision 6

02 OHP 5030.050-001 Main Turbine Oil Overspeed Operability Revision 1

Check

02 OHP 5030-050-002 Main Turbine Overspeed Test Revision 0

Letter AEP NRC 1168A Technical Specification Change Request to February 15, 1994

Delete Turbine Overspeed Protection

Requirements

Cook Plant Operations Review Committee February 16, 2002

Meeting Minutes

Unit 2 Caution Tag Log March 18, 2002

CR 98-06995 Unit 1 West Essential Service Water November 13, 1998

(ESW) Pump Room Supply Fans Are

Freewheeling Opposite of the Direction for

Rotation Indicated by Rotation Arrow

Mounted on Fan Housing

CR 99-02455 Residual Heat Removal Pumps May Be February 11, 1999

Experiencing Cavitation

CR 99-07602 Calculation PS-4KVD-002 Shows That the April 5, 1999

Momentary Ratings on the 4 KV Circuit

Breakers Are Exceeded for Fault

Conditions

CR 99-15072 4 KV Degraded Voltage Relay Technical June 9, 1999

Specification Lower Allowable Limit Is Not

Adequate to Protect Connected Safety

Related Motors

46

CR 99-17063 The Acceptance Criteria for Filter Maximum June 28, 1999

Allowable Pressure in Procedure

01-OHP-5030.001.001 Is Not Consistent

With Maximum Pressure Considered in

Calculation DCCHV12FH01S

CR 99-29182 A Revised Control Room Dose Analysis December 15, 1999

From Westinghouse Will Be Submitted to

the NRC for Their Approval

CR 00-01079 The Supply Air to the Valve Actuators of January 20, 2000

1/2-CCR-460, 1/2-CCR-462, 1/2-CRV-412

Exceeds the Manufacturer's Maximum

Allowable Casing Pressure

CR 00-01973 Existing Unit 2 Small Bore Piping Concerns February 2, 2000

That Resulted in Post Restart Design

Changes Based on Operability Criteria

CR 00-02125 Unit 2 Large Bore Piping Modifications February 4, 2000

Which Were Identified in the 02-DCP-0164

and 02-DCP-0647 and Most of These

Modifications Will Be Implemented Post

Restart

CR 00-03032 Some of the Small Bore CCW Piping February 22, 2000

Attached to the Reactor Coolant Pump

Thermal Barrier Is Not Adequately

Supported to Accommodate the Thermal

Movement of the Pumps

CR 00-07070 Calculation MD-12-CCW-818-N, May 16, 2000

Revision 0, Does Not Evaluate the Outside

of Containment Forged Head Assembly

CR 00279011 The Evaluation for CR 00-6696 Improperly October 5, 2000

Evaluated the Possibility of Hydraulic

Locking in Non-essential Service Water

Containment Isolation Valves

CR 01032027 Current Procedures Preferentially Align February 1, 2001

Residual Heat Removal System to

Flowpaths That Do Not Have the Required

Ventilation From the Hot Sleeve Ventilation

System

CR 01275031 During Unit 2 ESW Flow Verification October 2, 2001

Testing, ESW Flow to the Unit 2 West

CCW Heat Exchanger Was 30.4 GPM

Below the Acceptance Limit of 5520.6 GPM

47

CR 02036021 Document an Aggregate Operability February 5, 2002

Determination Evaluation to Support Unit 2

Restart Following the February 2002

Refueling Outage

CR 02050022 Control Switch 1-101-NRV-152 May Not Be February 19, 2002

in the Automatic Position Fully

CR 02057005 During Performance of February 22, 2002

02-OHP-5030-050-001, an Actual Turbine

Trip Occurred on the Second Attempt at

Overspeed Operability Checks

1R17 Permanent Plant Modifications

2-DCP-4821 Install New Impellers in the Containment Revision 0

Spray Pumps (2-PP-9E&W)

Design Change East Containment Spray Pump Revision 0

Package Procedure Performance and Flow Test

02-DCP-4821-TP.1

Calculation Unit 2 Emergency Core Cooling System Revision 1

MD-02-ECCS-005-N Pumps Net Positive Suction Head Analysis

Calculation Spray Additive Eductor Performance Revision 3

MD-12-CTS-117-N

Calculation Minimum Operability Limits for Revision 1

MD-12-CTS-135-N Containment Spray Pumps

JO 01102007 2-DCP-4821: 2-PP-9E, Install 5 Vane February 19,2002

Impeller

CR 02040037 During Pump Performance Run of 2-PP-9E February 9, 2002

East Containment Spray Pump Per

2-DCP-4821-TP.1, the Pump Developed

Head Was less than the Acceptance

Criteria

1R19 Post Maintenance Testing

Administrative Emergency Diesel Generators

Technical Requirement

2-EDG-1

01 OHP 4030-119-022E East Essential Service Water System Test Revision 2

48

12 IHP 6030-RLY-008 ABB Solid State Differential Relay Type Revision 0,

87M Series 419M Calibration and Change 0

Maintenance

12 IHP 6030-RLY-009 ABB Solid State Differential Relay Type Revision 2a,

87T Series 419 Calibration and Change 0

Maintenance

12 MHP 5021-001-023 Manual Diaphragm Valve Maintenance Revision 6,

Change 12

PMP 4043.SLV.001 Sealed/Locked Valves Revision 4

PMP 2291.PMT.001 Work Management Post Maintenance Revision 2

Testing Matrices

PMP 2291.TRS.001 Troubleshooting Plan for 2 CD Diesel February 8, 2002

Data Sheet 1 Generator Speed Variations

(CR 02039004)

Vendor Manual ITT Engineered Valves Maintenance and Revision 0

VTD-ITEV-0016 Instruction Manual for Handwheel

Operated Diaphragm Valves

Vendor Manual DIA-FLO Diaphragm Valves Installation, Revision 0

VTD-ITEV-0017 Operation, and Maintenance Manual

Vendor Manual DIA-FLO Handwheel Operated Diaphragm Revision 2

VTD-ITEV-0027 Valves

Engineering Programs Safety Related Pump In-service Test Revision 73

Technical Data Book, Hydraulic Reference

Figure 1-15.1

Engineering Programs Safety Related Pump In-service Test Revision 65

Technical Data Book, Vibration Reference

Figure 1-15.2

JO 01094018 2-CS-369, Replace Diaphragm February 22, 2002

JO 01225007 2 CD Diesel Generator Returned Fuel February 11, 2002

Injection Linkage to Approved

Configuration

JO 01262081 Rebuild the Unit 1 East ESW Pump March 13, 2002

1-PP-7E

JO 01323026 Investigate Motor Electrical Short of March 13, 2002

1-PP-7E

JO 02032010 Perform Overcurrent Testing on February 20, 2002

2-EZC-C-2B

49

JO 02039004 Troubleshoot/Repair 2-OME-150-CD February 12, 2002

Control Circuitry

JO 02047020 Replace 24 Volt DC [Direct Current] Power January 2, 2002

Supply PS2 at 2-PS-CGC-19

JO 02049054 Troubleshoot and Repair 600 Volt Supply February 21, 2002

Breaker to the Unit 2 CD2 Battery Charger

That Tripped Twice

JO 02049080 Investigate, Calibrate, Replace Relay February 19, 2002

2-87-DGCD-3 As Required

JO 02050025 Investigate, Calibrate, Replace Relay February 20, 2002

2-87-T21C-1 As Required

JO 02050026 Investigate, Calibrate, Replace Relay February 20, 2002

2-87-T21D-1 As Required

JO R0208707 Calibrate East ESW Header Pressure March 12, 2002

Switch

JO R0209205 Calibrate Time Delay Relays for East ESW March 12, 2002

Pump Strainer

Dedication Plan Inspection and Refurbishment of Revision 7

HP-0035 Emergency Diesel Generator Governor or

Procurement of New Governor

CR 97-3562 SOER [Significant Operating Event Report] December 10, 1997

97-1, Potential to Gas Bind Pumps

Providing Safety Boron Injection Function

CR 02039033 Between February 2, 2002 and February 3, February 8, 2002

2002 There Were Ten CRs Initiated to

Document Snubbers Installed Backwards

CR 02042009 Dedication Plan HP-0035 Needs to Be February 11, 2002

Revised

CR 02047050 The Unit 2 West CCP Showed Signs of Air February 16, 2002

Entrainment During Attempts to Swap

CR 02047051 Check Stem Nut Setting on 2-CS-369 February 16, 2002

CR 02049054 The CD2 Battery Charger Failed to Control February 18, 2002

Bus Voltage Resulting in Multiple Control

Room Annunciators and a Large Current

Loading on the Charger

CR 02049057 CD Battery Ground February 18, 2002

CR 02049063 Observed Electrical Flash From 2-RPST-B February 18, 2002

50

CR 02049080 During Investigation for 2-BC-CD-2, Found February 18, 2002

2-87-DGCD-3 Relay As a Possible Issue

for Repairs

CR 02049081 Per 2-BC-CD-2 Battery Charger February 18, 2002

Troubleshooting, Need to Investigate Unit 2

Solid State Protection System Equipment

for Possible Damage

CR 02050025 Test, Repair, or Replace as Necessary, the February 19, 2002

Differential Relays for Transformer TR21C

Following the 250 Volt DC System Anomaly

on February 18, 2002

CR 02050026 Test, Repair, or Replace as Necessary, the February 19, 2002

Differential Relays for Transformer TR21D

CR 02050050 Verify Correct Stem Nut Setting on Valve February 19, 2002

1-CS-369

CR 02072061 During the Coupled Run on the 1E ESW March 13, 2002

Pump the Instantaneous Overcurrent

Alarm Came in and Smoke Was Noted at

the Motor Termination Box

CR 02080039 NRC Identified That Post Maintenance March 21, 2002

Testing Specified in JO 02039004 Did Not

Incorporate the Guidance Contained in

PMP 2291.PMT.001 for Post Maintenance

Testing Following Actuator Replacement

1R20 Refueling and Outage Activities

D.C. Cook Nuclear Plant Unit 2 Technical

Specifications

D. C. Cook Nuclear Plant Updated Final

Safety Analysis Report

02-OHP-4021-001-001 Plant Heatup From Cold Shutdown to Hot Revision 26, C3

Standby

02-OHP-4021-001-002 Reactor Start-Up Revision 22, C0

02-OHP-4021-001-006 Power Escalation Revision 19, C0

2-OHP-4030-STP-041 Refueling Integrity Revision 8

12-EHP-4030-002-356 Lower Power Physics Testing With Revision 0A, C1

Dynamic Rod Worth Measurement

51

12-MHP-4030.031.001 Inspection of Lower Containment and Revision 0, C1

Recirculation Sumps

PMP 4100-SDR-001 Plant Shutdown Safety and Risk Revision 5, C1

Management

Daily Shift Managers Logs February 10, 2002

through

February 28, 2002

Memo From R.W. Unit 2 Time to 200EF and Time to Boil January 4, 2002

Hennen to Shift Figures for the Refueling Outage

Technical Advisors

U2C13 Outage Schedule Shutdown Risk

Review

D. C. Cook Unit 2 2000 Final Core Map

D. C. Cook Unit 2 Cycle 13 Final Core Map

D. C. Cook Unit 2 Cycle XII - XIII Core

Unload Fuel Handling Movement Sequence

D. C. Cook Unit 2 Cycle XII - XIII Core

Reload Fuel Handling Movement Sequence

D. C. Cook Unit 2 Cycle 13 Core Operating Revision 0

Limits Report

JO R0203029 549 Day Surveillance for Unit 2 February 13, 2002

Containment Sumps

Drawing 12-3902A-0 Recirculation Sump & Screen Repair Revision 0

Containment Building Unit No. 1 & 2

Drawing 12-3902-9 Unit 1 & Unit 2 Containment Building Revision 9

Miscellaneous Frames

CR 02044004 NRC Identified Coating Degradation on February 13, 2002

Nuts Holding Level Instrumentation Well

Lateral Support Brackets

CR 02044006 NRC Identified Screens Had a Gap Larger February 13, 2002

Than the 1/4 Inch Requirement Allowed

Per Procedure 12-MHP-4030.031.001

CR 02044060 JO 195371-02 Was Taken to Complete February 13, 2002

Status Without Performing the Required

Protective Coatings in the Recirculation

Sump

52

CR 02058037 Corrupted Computer File Results in February 27, 2002

Incorrect Measured Control Rod Worth

During Low Power Physics Testing

1R22 Surveillance Testing

D.C. Cook Nuclear Plant Unit 2 Technical

Specifications

D. C. Cook Nuclear Plant Updated Final

Safety Analysis Report

Updated Final Safety Emergency Power System Revision 17

Analysis Report,

Section 8.4

Technical Specification Engineered Safety Feature Actuation Amendment 187

3.3.2.1 System Instrumentation

Administrative Emergency Diesel Generators Revision 10

Technical Requirement

2-EDG-1

Rapid Event Response Report for January 21, 2002

CR 02020031

02-OHP 4030-001-002 Containment Inspection Tours Revision 13

02-OHP 4030-202-060 Pressurizer Relief Valve Testing Revision 0, C0

02-OHP DG2CD Load Sequencing & ESF Testing Revision 3

4030-232-217A

02-OHP East Containment Spray System Revision 16

4030.STP.007E Operability Test

Design Information Test Procedure Acceptance Criteria for Revision 6

Transmittal (DIT) Containment Spray Pumps (1(2)-PP-9E,

B-00770 &9W)

DIT-B-01542 Acceptable Back-leakage Flow Rate Revision 0

Through 2-CTS-120E with Regards to

Containment Spray and Recirculation

Sump pH Analysis

DIT-B-01544 Acceptable Back-leakage Flow Rate Revision 1

Through Spray Additive Tank Check

Valves with Regards to Containment Spray

and Recirculation Sump pH Analysis

53

DIT-B-02327 Stroke Time Acceptance Criteria for Revision 0

1(2)-NRV-152, -153

Calculation Determination of Available Pressurizer Revision 1

MD-12-CA-004-S Power Operated Relief Valve Strokes

Using the Auxiliary Air Supply

Calculation Spray Additive Eductor Performance Revision 3

MD-12-CTS-117-N

Calculation Minimum Operability Limits for Revision 1

MD-12-CTS-135-N Containment Spray Pumps

Engineering Programs Safety Related Pump In-service Test Revision 59

Technical Data Book, Hydraulic Reference

Figure 2-15.1

Engineering Programs Power Operated Relief Valve Stroke Time Revision 52

Technical Data Book, Limits

Figure 2-19.1

Engineering Programs Power Operated Relief Valve Stroke Time Revision 53

Technical Data Book, Limits

Figure 2-19.1

Engineering Programs Diesel Generator Pot Settings Revisions 30 & 31

Technical Data Book,

Figure 2-19.9

Flow Diagram Containment Spray Unit 2 Revision 50

OP-2-5144

Clearance Order Isolate West Containment Spray Pump February 16, 2002

2012025

CR 01173001 The Vibration Alert Limits Are Higher Than June 21, 2001

the Action Limits for the #2 Boric Acid

Transfer Pump

CR 01255059 TDB Figure 2-15.1 Allows CCP Interaction September 12, 2001

Delta Pressure In Excess of Design Basis

Calculation

CR 01270017 Untimely Engineering Evaluation, Resultant September 27, 2001

Re-baseline Determination, and TDB

Change for Power Operated Relief Valve

(PORV) 1-MRV-213 Delayed the Unit 1

Ascension to Mode 4

CR 01292027 Non-conservative Acceptance Criteria in October 19, 2001

TDB Figure 2-15.1 for 2-PP-26N

54

CR 01324040 Non-conservative Acceptance Criteria in November 20, 2001

TDB Figure 2-15.1 for 2-PP-10E

CR 02046013 Containment Annulus Pipe Tunnel Sump February 15, 2002

Pump 2-PP-61A Did Not Meet Acceptance

Criteria at Step 5.1.5 of Surveillance

Procedure 2-EHP-4030-231-240 for GPM

CR 02046050 NRC Identified Unit 2 Pressurizer PORVs February 15, 2002

2-NRV-152 & 153 Were Retested Using

TDB Stroke Times and a Testing

Procedure That Had Not Been Revised to

Contain the Corrective Actions to Ensure

Operability In Accordance With Information

Contained in DIT-B-02327-00

CR 02050067 NRC Identified Minor Quantities of Debris February 19, 2002

in Lower Ice Condenser Following Unit 2

Refueling Outage

CR02051076 Resident Inspector Identified Dry Boric Acid February 20, 2002

on 2-IRV-120

CR 02051077 NRC Identified Dry Boric Acid at the Pipe February 20, 2002

Caps of Valves 2-CS-441-1 and

2-CS-441-2

CR 02051078 NRC Identified Dry Boric Acid on February 20, 2002

Transmitter 2-NFP-212

CR 02052001 NRC Identified Dry Boric Acid on Valve February 21, 2002

2-NPI-110-V1

CR 02052002 NRC Identified Dry Boric Acid on Valve February 21, 2002

2-IMO-54

CR 02052003 NRC Identified Dry Boric Acid on Valve February 21, 2002

2-CS-450-4

CR 02052008 NRC Identified Dry Boric Acid on February 21, 2002

Containment Spray Header Piping

CR 02052010 NRC Identified Containment Inspection February 21, 2002

Tour Deficiencies Following Unit 2

Refueling Outage

CR 02052039 NRC Identified That Abandoned Conduit February 21, 2002

Left in Containment Contrary to Design

Change Instructions

CR 02053063 NRC Identified Minor Equipment Storage February 22, 2002

Deficiencies in the Auxiliary Building

55

1R23 Temporary Plant Modifications

D. C. Cook Nuclear Plant Updated Final

Safety Analysis Report

Temporary Modification Installation of Noise Filtering Resistors on November 16, 2001

2-TM-00-54-R1 Cables 2-4450PB-2 for 2-ILA-111 and

2-5658PB-2 for 2-ILA-121

12-EHP-5040-MOD-001 Temporary Modifications Revision 9

JO 01320005 Install Temporary Modification November 17, 2001

2-TM-00-54-R1 on Cable 2-4450PB-2 for

2-ILA-111

10 CFR 50.59 Safety Original Revision of 2-TM-00-54-R0, September 19, 2000

Screening Installation of Noise Filtering Resistor on

2000-1940-00 Cable 2-5658PB-2 for 2-ILA-121

10 CFR 50.59 Revision to Temporary Modification November 16, 2001

Applicability 2-TM-00-54-R1 to Include Cable

Determination 2-4450PB-2 for 2-ILA-111

2001-1408-00

Memo from T. Craven Waiver of Design Review Board for November 16, 2001

to D. Hafer 2-TM-00-54-R1

CR 01355035 Replace the Currently Installed Foxboro December 21, 2001

Accumulator Level Alarm Transmitter With

an Equivalent Rosemont Transmitter

CR 02086013 Lost Implementation Checklist (Data March 27, 2002

Sheet 8 of Temporary Modification

Procedure 12-EHP-5040-MOD-001,

Revision 8) for Temporary Modification

2-TM-00-54, "Installation of Noise Filtering

Resistors on Cable 2-4450PB-2 for

2-ILA-111"

2OS1 Access Controls For Radiologically Significant Areas

PMP-6010-RPP-003 High, Locked High, and Very High Revision 10

Radiation Area Access

CR 02029056 Unit-2 Reactor Head Set High Radiation January 29, 2002

Area Posting

56

CR 02025007 Access to Restricted Areas Poorly January 25, 2002

Controlled During RCS [Reactor Coolant

System] Cleanup Post Shutdown

2OS2 ALARA [As Low As Reasonably Achievable] Planning and Controls

U2C13 RWP [Radiation Work Permit] Dose January 20, 2002

Totals Reports and Cook Plant Daily through

ALARA Reports February 7, 2002

Listing of Outage Generated CRs Coded to January 19, 2002

RP [Radiation Protection] Issues through

February 7, 2002

PMP-6010.ALA.001 ALARA Program - Review of Plant Work Revision 11

Activities

12-THP-6010.RPP.006 Radiation Work Permit Processing Revision 17

12-THP-6010-RPP-018 Controls for Radiological Risk Significant Revision 0

Work Activities

RWP # 022136 and Scaffold Activities in the Containment and RWP Revision 05

Associated ALARA Plan Auxiliary Buildings

RWP # 022170 and U2C13 DCP 525 - Modify/Replace RWP Revision 05

Associated ALARA Plan Pressurizer Spray Line Temperature

Sensor

RWP # 022119 and Temporary Shielding RWP Revision 02

Associated ALARA Plan

RWP # 022152 and CRDM [Control Rod Drive Mechanism] RWP Revision 00

Associated ALARA Plan Inspections

RWP # 022134 and Containment Insulation RWP Revision 02

Associated ALARA Plan

RWP # 022140 and Steam Generator & Diaphragm Activities RWP Revision 00

Associated ALARA Plan

RWP # 022141 and Steam Generator Primary Work - Platform RWP Revision 08

Associated ALARA Plan Activities

PMP-6010.ALA.001 ALARA In-Progress Review for Scaffold January 22, 24 and

Support Activities February 1, 2002

PMP-6010.ALA.001 ALARA In-Progress Review for Pressurizer February 5, 2002

Spray Line Temperature Sensor

Replacement

57

PMP-6010.ALA.001 ALARA In-Progress Review for Steam February 4, 2002

Generator Primary Activities

CR 02019069 Reactor Flood Up Specification - Shutdown January 19, 2002

Chemistry

CRs 02022024, Radworker [Radiation Worker] January 19, 2002

02029013, 02019072, Performance Related Issues through

02020020, 02020021, February 7, 2002

02022024, 02021064,

02021065, 02023006,

02023008, 02024011,

02023043, 02028039,

02029013, 02029016,

02033063, 02033066,

02034034, 02035008,

02038002

CR 02031019 Additional Dose During Scaffold Work January 31, 2002

CR 02025001 Scaffold Activities January 25, 2002

TEDE [Total Effective Relocate Temperature Sensor; Under Various dates

Dose Equivalent] Reactor Head Inspections; Insulation between

ALARA Evaluations For Removal; Steam Generator Manway November 28, 2001

RWP #s 02-2170; Activities; and Steam Generator Eddy and January 24,

02-2152; 02-2134; Current Activities 2002

02-2140; and 02-2141

Rad/Chem - Readiness of ALARA Outage Planning for August 2001

Environmental U2C13

Department

Self-Assessment

Report

SA-2001-RPS-009

Performance Field Observations # 01-L-043, 02 A-003, Various dates

Assurance Field 01-L-036, 01-K-061, 01-F-032, 01-K-040, between

Observations 02-A-072, 02-A-112, 02-A-081, 02-A-107, November 14, 2001

02-A-117, 02-B-005, 02-A-109, 02-A-130, and February 4,

02-A-026, 02-A-122, 02-A-124 2002

CR 02029016 and Individual Disregarded RP Technician January 29, 2002

related preliminary Directive and ED Dose Alarm While and related

investigation Working in U2 Lower Containment information through

information January 31, 2002

12-THP-6020-CHM-110 RCS Chemistry - Shutdown/Refueling Revision 8(c)

D.C. Cook Nuclear Power Plant 2001 Dose December 2001

Reduction Five Year Plan

58

4OA1 Performance Indicator Verification

02 OHP 4025.001.001 Emergency Remote Shutdown Revision 3

02 OHP 4022-055-003 Loss of Condensate to Auxiliary Feedwater Revision 6a

Pumps

02 OHP 4025.LS-2 Start-Up AFW [Auxiliary Feedwater] Revision 0

02 OHP 4025.LS-3 Steam Generator 2/3 Level Control Revision 1

JO 02018064 2-PP-4 TDAFWP [Turbine Driven Auxiliary February 19, 2002

Feedwater Pump] Tripped Shortly After

Startup

DIT-S-01037 Auxiliary Feedwater Pump Steam Turbine Revision 1

Drive Trip and Throttle Valve Latch Hook

Linkage Machining Information

Receipt Inspection Report May 27, 1986

Purchase Order/Contract 03157-821-5X

CR 01222001 While Performing Fill and Vent Procedure August 10, 2001

for the TDAFWP, the Pump Failed to Start

CR 01354104 Prompt Operability Determination for Both December 20, 2001

Units TDAFWPs. Trip Throttle Valve Latch

Faces Have Not Been Maintained as Per

Vendor Information

CR 02018064 TDAFWP Trip Throttle Valve Tripped January 18, 2002

Shortly after Start of the Pump During

Performance of Time Response Test

CR 02019071 Performance Assurance Identified That January 19, 2002

Operability Determination for CR 02018064

and CR 01354104 for the TDAFWP Were

Inadequate

4OA3 Event Followup

D.C. Cook Nuclear Plant Unit 1Technical

Specifications

D.C. Cook Nuclear Plant Unit 2 Technical

Specifications

59

Licensee Event Report Failure to Perform Increased Frequency

(LER) Surveillance on 2 East Containment Spray

50-316-2000-012-00 Pump

LER Failure to Perform Increased Frequency

50-316-2000-012-01 Surveillance on 2 East Containment Spray

Pump, Supplement 1

LER Power Range Nuclear Instrumentation

50-315-2001-002-00 Calibration Procedure Not in Conformance

with Technical Specifications

60