IR 05000315/2021010

From kanterella
Jump to navigation Jump to search
Biennial Problem Identification and Resolution Inspection Report 05000315/2021010 and 05000316/2021010
ML21245A413
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 09/07/2021
From: Nestor Feliz-Adorno
Reactor Projects Region 3 Branch 4
To: Gebbie J
Indiana Michigan Power Co
References
IR 2021010
Download: ML21245A413 (16)


Text

SUBJECT:

DONALD C. COOK NUCLEAR PLANT - BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000315/2021010 AND 05000316/2021010

Dear Mr. Gebbie:

On August 5, 2021, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at your Donald C. Cook Nuclear Plant. On August 5, 2021 the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspection team reviewed the stations corrective action program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

The team also evaluated the stations processes for use of industry and NRC operating experience information and the effectiveness of the stations audits and self-assessments.

Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

Finally, the team reviewed the stations programs to establish and maintain a safety-conscious work environment and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews the team found no evidence of challenges to your organizations safety-conscious work environment.

Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

No findings or violations of more than minor significance were identified during this inspection.

September 7, 2021 This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Néstor J. Féliz Adorno, Chief Branch 4 Division of Reactor Projects Docket Nos. 05000315 and 05000316 License Nos. DPR-58 and DPR-74

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000315 and 05000316

License Numbers:

DPR-58 and DPR-74

Report Numbers:

05000315/2021010 and 05000316/2021010

Enterprise Identifier:

I-2021-010-0045

Licensee:

Indiana Michigan Power Company

Facility:

Donald C. Cook Nuclear Plant

Location:

Bridgman, MI

Inspection Dates:

July 19, 2021 to August 05, 2021

Inspectors:

E. Fernandez, Reactor Inspector

J. Mancuso, Resident Inspector

R. Ng, Project Engineer

G. O'Dwyer, Reactor Engineer

Approved By:

Néstor J. Féliz Adorno, Chief

Branch 4

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at Donald C. Cook Nuclear Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the coronavirus (COVID-19), inspectors were directed to begin telework. In addition, regional baseline inspections were evaluated to determine if all or a portion of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on site. The inspections documented below met the objectives and requirements for completion of the IP.

OTHER ACTIVITIES - BASELINE

71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 02.04)

(1) The inspectors performed a biennial assessment of the licensees corrective action program, use of operating experience, self-assessments and audits, and safety conscious work environment.

Corrective Action Program Effectiveness: The inspectors assessed the corrective action programs effectiveness in identifying, prioritizing, evaluating, and correcting problems. The inspectors also conducted a five-year review of the ice condenser glycol chiller system.

Operating Experience, Self-Assessments and Audits: The inspectors assessed the effectiveness of the stations processes for use of operating experience, audits and self-assessments.

Safety Conscious Work Environment: The inspectors assessed the effectiveness of the stations programs to establish and maintain a safety-conscious work environment.

INSPECTION RESULTS

Assessment: Assessment of the Corrective Action Program 71152B Based on the samples reviewed, the team concluded that the licensee's implementation of the Corrective Action Program was generally effective and supported nuclear safety.

Effectiveness of Problem Identification:

Based on the samples reviewed, the team concluded that the licensee continued to identify issues at a low threshold and appropriately entered these issues into the Corrective Action Program. The team determined that the licensee usually entered problems into the Corrective Action Program completely and accurately. The inspectors determined that the station was generally effective at identifying negative trends that could potentially impact nuclear safety.

The team also noted that some deficiencies were identified by external organizations, including the NRC, that had not been previously identified by licensee staff and were subsequently entered into the Corrective Action Program. In addition, the licensee also utilized Corrective Action Program support processes to identify problems, including the self-assessment and audit process and the Operating Experience Program. For example, the licensee performed department self-assessments and quality assurance audits to identify issues in station processes. Similarly, the licensee screened issues from both NRC and industry operating experience and entered them into the Corrective Action Program when they were applicable to the station.

The team determined that the licensee was generally effective at trending low-level issues and taking appropriate corrective actions to prevent more significant problems from developing. In addition, the licensee used the Corrective Action Program to document instances in which previous corrective actions were ineffective or were inappropriately closed.

The team performed a 5-year review of the ice condenser glycol chiller issues. As part of this review, the team interviewed the system engineer, reviewed the plant health report, and reviewed selected corrective actions and condition evaluation documents. The team concluded that the ice condenser glycol chiller concerns were identified and entered into the Corrective Action Program at a low threshold and were resolved in a timely manner commensurate with their safety significance. The team did not identify any additional issues.

Effectiveness of Prioritization and Evaluation of Issues:

Based on the samples reviewed, the team determined that licensee performance was generally effective at prioritizing and evaluating issues commensurate with the safety significance of the identified problem. The Initial Screening Committee and the Management Screening Committee meetings were generally thorough and intrusive in reviewing issues and prioritizing actions. In addition, the team observed a healthy dialogue between the members of these committees and the members challenged each other when dispositioning issues.

In general, once a degraded or non-conforming condition was identified, the Corrective Action Program directed that an equipment operability or functionality review be performed. As a result, most of the samples reviewed were evaluated in a timely manner. However, the team noted examples of condition reports that had less than adequate documentation of evaluation activities. The details of this issue are documented in the observation section below.

Effectiveness of Corrective Actions:

Based on the samples reviewed, the team determined that the licensee was generally effective in corrective action implementation. In general, corrective actions for deficiencies that were safety significant were implemented in a timely manner. Problems identified using a root cause or other cause methodologies were resolved in accordance with Corrective Action Program requirements. The team determined that the licensee generally assigned corrective actions that were effective and timely for NRC identified issues and licensee event reports (LERs).

Assessment: Use of Operating Experience 71152B Based on the samples reviewed, the team determined that licensee's performance in the use of operating experience was generally effective. The licensee screened industry and NRC operating experience information for applicability to the station. The team observed the Operating Experience Screening Committee meeting and determined that the licensee initiated actions in the Corrective Action Program to fully evaluate the impact, if any, to the station. When applicable, actions were developed and implemented to prevent similar issues from occurring. Operating experience lessons learned were communicated and incorporated into plant operations. The team observed the information being used in daily activities, such as pre-job briefs, as well as issue reviews and investigations. The team did not identify any concerns in this area.

Assessment: Self-Assessments and Audits 71152B Based on the samples reviewed, the team determined that the licensee's performance of self-assessments and audits was generally effective. The licensee performed department self-assessments and nuclear oversight audits throughout the organization on a periodic basis. These self-assessments and audits were generally effective at identifying issues and enhancement opportunities at an appropriate threshold. The self-assessments and audits reviewed by the team identified issues that were not previously known, including issues within the Corrective Action Program itself. The licensee's Nuclear Oversight (NOS) identified deficiencies with the licensee's processes and those issues were addressed by the station through the Corrective Action Program. The team did not identify any concern in this area.

Assessment: Safety Conscious Work Environment 71152B The team reviewed the results from the 2019 Employee Concerns Annual Assessment, the 2019 and 2020 departmental safety culture surveys and the 2020 Gallup survey. The team also conducted one-on-one interviews with 23 licensee staff concerning the effectiveness of the Corrective Action Program, the ability to raise issues, and the freedom from potential retaliation for raising issues. The team did not identify any impediment to the establishment of a safety conscious work environment.

In general, the licensee's staff was aware of and familiar with the Corrective Action Program and other processes to raise nuclear safety concerns, such as the Employee Concerns Program. Licensee staff indicated they could raise nuclear safety concerns without a fear of retaliation. The team did not identify examples of retaliation for raising nuclear safety concerns. The licensee staff interviewed believed that operational issues and issues with high safety significance were being appropriately addressed in a timely manner.

Minor Violation: Failure to Follow the Operability Evaluation Procedure 71152B Minor Violation: In 2015, an NRC Component Design Bases Inspection identified a finding for the licensees failure to appropriately establish the in-service inspection boundaries for the safety-related component cooling water system. As part of the corrective actions, the licensee performed Engineering Change (EC) 56391 to upgrade steam generator sample coolers 1-QC-501-6 and 2-QC-501-9 from Seismic Class III to Seismic Class I.

On March 4, 2019, during the walkdown being performed in support of this EC, the licensee noted that support for cooler 1-QC-501-6 was missing the bottom unistrut bolt and support for cooler 2-QC-501-9 was missing a top mounting bolt. The licensee initiated AR 2019-1940 to document the missing bolts. The shift manager stated in the operability review section of the AR that an operability justification was not required because the support was Seismic Class III (not safety related). The licensee also created Work Order Task 55529607-01 to replace the bolts.

In May 2019, the missing top mounting bolt on cooler 2-QC-501-9 was replaced. However, the missing bottom unistrut bolt on cooler 1-QC-501-6 was not accessible and therefore not replaced. The work order was subsequently closed in June 2019.

In January 2020, the licensee discovered that the work order was closed and wrote AR 2020-0255 to ask Engineering to accept the condition as-is. However, engineering stated in the AR that evaluating the acceptance of the missing bolt as-is required significant engineering resources. Therefore, work order 55561980 was initiated to replace the missing bolt, which was in planning status at the time of this inspection.

During this inspection, the team noted the licensee incorrectly treated the affected piping section as Seismic Category III when evaluating the need to perform an operability determination. Procedure PMP-7030-OPR-001, Operability Determination, Revision 37, required an operability evaluation for Seismic Class I components such as this piping section.

The team determined that the failure to follow this procedure was a performance deficiency and a violation of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings."

Screening: The inspectors determined the performance deficiency was minor. The performance deficiency was minor because it did not adversely affect the mitigating systems cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the deficiency did not result in reasonable doubt about the equipments seismic qualifications as the licensee did not have to revise any calculation or evaluation to resolve the associated operability concerns.

Enforcement:

This failure to comply with 10 CFR50 Appendix B, Criterion V, constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy.

Observation: Lack of Technical Rigor in Corrective Action Program Evaluation 71152B The team noted examples of lack of technical rigor in corrective action program evaluations, including:

The licensees audit determined a vendors quality assurance program was ineffective as documented in AR 2019-12088. The licensee removed the vendor from the Approved Suppliers List / Quality Suppliers List and concluded items received from that vendor after January 2017 required additional quality evaluation for acceptance or rejection. The licensee also determined that a sight glass provided by this vendor was installed on the oil reservoir for the Unit 1 east charging pump 1-PP-50E. The licensee performed discrepant condition evaluation (DCE) 2020-0390 to evaluate the impact of the non-qualified sight glass to the charging system and initiated work order 55542705 to replace the sight glass with a quality-related part. The DCE concluded that the sight glass had the same form, fit and function as a quality assurance (QA)qualified installation. Therefore, the licensee concluded that the part would maintain the required integrity with no additional justification. However, the team concluded the DCE did not provide sufficient technical justification because it did not consider relevant attributes such as seismic qualifications, material properties and equipment qualification (EQ) as the licensee would have to perform for the unqualified spare parts. The inspectors determined there was no significant safety impact since the sight glass was replaced within a reasonable amount of time.

The licensee generated AR 2020-4967 for degraded essential service water piping due to flow accelerated corrosion. The licensee determined that the minimum allowable wall thickness criteria established in procedures for certain areas were non-conservative due to the presence of welded piping attachments. The licensee created assignments to correct the calculations, revise the affected inspection procedures, and review the extend of condition. However, the team noted the licensee did not establish an interim action until the procedures were revised. The licensee entered this issue into the corrective action program as AR 2021-6742 and planned to revise the affected procedures to add interim guidance. The licensee did not identify examples of unacceptable wall thickness that were deemed acceptable due to the non-conservative acceptance criteria.

The licensee failed to perform an operability evaluation because it incorrectly determined the affected component was Seismic Class III (not safety related). This issue was documented as a minor violation in this inspection report.

The inspectors concluded that the lack of technical rigor in corrective action program evaluation represented a weakness in addressing deficient conditions. The licensee entered this issue into the corrective action program as AR 2021-7077.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On August 5, 2021, the inspectors presented the biennial problem identification and resolution inspection results to you and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Security Survey Results

07/2019

Material Management Survey Results

08/2019

Chemistry/Environmental Survey Results

11/2019

Work Control and Schedule Survey Results

09/2020

2010-11114

Exposed Insulation Found During U2C19 Recirc Sump

Walkdown

10/19/2010

2013-13536

NRC Comment on Methodology of Vortex Calculations

09/13/2013

2013-16557

Cable Tray and Conduit Overfill Issues

10/28/2013

2014-14190

Failure of 2D5 Synch Circuit

11/12/2014

2014-15099

Identified a Pin Hole Leak in 2-HV-AFP-EAC ESW Piping

10/02/2014

2015-4459

ISI-Scope Deferral for U2C22

03/31/2015

2016-12216

U2C23 Baffle-Former Bolt UT Inspection Results

10/23/2016

2016-1537

AR 2016-1537 Plant and Drawing Configuration Discrepancy

for Condensate System

2/08/2016

2016-7752

PRT Seismic Anchor Movement

06/30/2016

2017-11986

1SI-158-L2/L3 Leakage Above Acceptance Criteria

11/22/2017

2017-4740

Loss of CCS Charging Warrants an AOP

05/09/2017

2017-7596

Floor Drain Credited in Fire Modeling Are Not Monitored

08/07/2017

2017-9084

AR 2017-9084, 12-OME-129-9 Glycol Chiller #9 Trouble

Alarm

09/16/2017

20174-5989

N-Train Battery Charger Part Evaluation

06/15/2017

2018-10025

AR 2018-10025 Update Drawing Desktop Guide

10/30/2018

2018-1045

Missed Security Patrol

2/01/2018

2018-10451

NRC Inspection QHSA-71124.05 Rad Monitoring

Instrumentation

11/15/2018

2018-11245

2-DR-GCS2 Missing Required Door Sweep

2/17/2018

2018-6613

Inadequate Evaluation of LOCA Anchor Motions

06/26/2018

2018-7204

Deficiency of Evaluation of Emergency Level Conditions

07/17/2018

2018-9690

1-OME-150-AB Fuel Line Leak Near #6 Rear Fuel Injector

10/16/2018

2019-10855-4

Review Installation of Sight Glass in 1-PP-50E

01/14/2020

71152B

Corrective Action

Documents

2019-11077

Drop in Frequency Noted During LOP/LOCA Testing

11/07/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

2019-12088

Vendor Quality Program Ineffective

2/11/2019

2019-12191

GT 2019-12191, Cook Review of NRC IN-2012-22, Rev 1:

Counterfeit, Fraudulent, Suspect Item (CRSI) Training

Offerings

11/20/2019

2019-12255

Corrosion in Fire Protection Piping

2/17/2019

2019-1349

Bent Hanger in U2-East RHR Pump Room 2-GRH-V819

2/11/2019

2019-1398

Determine Impact (CDI) for Completion of SD-180820-001

2/12/2019

2019-4190

Air Void Per UT is Unacceptable Location Prior to 1-IMO-261

04/21/2019

2019-5275

Transcript Error of SRD Calibration

05/16/2019

2019-6691

Negative Trend of INPO Radiation Protection Events

Indicator

07/08/2019

2019-6882

AR 2019-6882, Unit 2 Ice Bed Temps above ESOMS

Notification Limits

07/15/2019

2019-6998

AR 2019-6998 Unexpected Alarm in Unit 2 Control Room

07/18/2019

2019-7047

Received a 204 Drop 13 South NESW PP Strainer DP High

07/21/2019

2019-7276

AR 2019-7276 Intermittent Alarm 2-SG-7 PT 162

07/27/2019

2019-8320

AR 2019-8320 Unit 2 ITS 5.5.12.d Specific Requirements

May Not Being Met

08/29/2019

20-0255

WOT 55529607 Was Not Completed as Prescribed

01/09/2020

20-0390

1-PP-50E, Replace Sight Glass Installed Under WO 55455925

01/13/2020

20-0529

Update Specs to Support Section XI Requirements

01/16/2020

20-10105

MTS UPS Condition Identified During PM

2/10/2020

20-10439

GT 2020-10439 Cook Review of IN 2020-004 - Operating

Experience Related to Failure of Buried Fire Protection Main

Yard Piping

2/23/2020

20-10440

GT 2020-10440 Cook Review of IN 2018-11, SUPPLEMENT

1: QA Record Falsification at Kobe Steel and Other

International Vendors 12/23/2020

2/23/2020

20-1047

ACE AR 2020-1047, Gland Seal Effluent RMS High Range

Reading

2/16/2020

20-1877

CCE AR 2020-1877 ERO Qualification Process and Tracking

in PQM

01/13/2021

20-2027

Failed Operations Surveillance

2/28/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

20-2642

ACE AR 2020-2642 Radiation Monitor Communication to

Control Room Lost

06/25/2020

20-3709

RCE CR 2020-3709 RCS Leak - Plug Unit 1 NRV-163/NRV-

164 Bellows Tell-Tale at the Bonnet

08/04/2020

20-3739

ACE AR 2020-3739, 2-NRI-32 is Slowly Failing Low

09/19/2020

20-4285

Actions are Not Always Changing Workflow State as

Required

05/20/2020

20-4891

AR 2020-4891, 1-VTR-185 High Temp Alarm

06/15/2020

20-4946

Wrong Radiation Work Permit used to Enter the U2 Vestibule

06/17/2020

20-4967

Degraded ESW Pipe Downstream of 1-WMO-715

06/17/2020

20-6117

NOS Identified Deficient Execution of Fire Door Surveillance

08/03/2020

20-7242

GT 2020-7242, Cook Review of IN 2020-02 - FLEX Diesel

Generator Operational Challenges

11/23/2020

20-8177

Performance Issues/Common Cause

10/05/2020

21-0169

Cook Review of IN 2007-21, Supplement 1: Pipe Wear Due

to Interaction of Flow-Induced Vibration and Reflective Metal

Insulation

01/06/2021

21-2008

CCE AR 2021-2008, Glycol Chiller Failure Possible Trend

04/28/2021

21-2838

CCE AR 2021-2838 Vulnerabilities introduced During Design

Modifications

04/05/2021

21-2858

AR 2021-2858 U2 Ice Condenser FME Walkdown

04/06/2021

21-3139

AR 2021-3139 Disparity in Unit 2 Source Range Readings

04/17/2021

21-4239

AR 2021-4239, 2-NRV-152 Failed as Found Stroke Time on

Backup Air

05/11/2021

21-4250

GT 2021-4250 Cook Opex Review of NRC IN 21-01,

Lessons Learned from NRC Inspections of Design-Basis

Capability of Power-Operated Valves at Nuclear Power

Plants

05/11/2021

21-4721

Steam/Water Leak on 2FW-115-4

05/21/2021

21-4722

DPM Condensate Leak

05/22/2021

21-4743

2-SV-1A-4 Steam Leak

05/23/2021

21-4750

Leak by on 1-CW-344E

05/23/2021

21-4812

Minor RCS Back Leakage Suspected Through 1-SI-152S

05/25/2021

21-4817

WR Only to Install Missing Clips on CCW Cooling Coils

05/25/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

21-4882

1-OME-34W Packing Leaks on Inlet and Outlet Valves

05/26/2021

21-5016

U2 CD EDG Coalescing Filter Air Leak

06/01/2021

GT 2020-10549

White Finding for Check Valve Not Meeting IST

Requirements

2/30/2020

GT 2021-1076

Perform OE Evaluation for James A Fitzpatrick Finding

2/01/2021

GT 2021-2166

Westinghouse Technical Bulletin TB-19-5 Rev. 1

03/09/2021

21-6378

Drawing Updated Prematurely and EDB Impacts Missed

07/22/2021

21-6638

Operability Review of CR 2019-1940 & Seismic Class

07/29/2021

21-6742

Interim Guidance Not Developed for UT Exam

08/03/2021

21-6785

Attachments Not Attached to AR 2019-1349-2

08/04/2021

21-6809

DIT / Calc Guidance for FAC Tmins Do Not Include WPA

Stresses

08/04/2021

21-7077

Observation of Technical Rigor in ENG Products

08/16/2021

Corrective Action

Documents

Resulting from

Inspection

21-7078

NRC Observation on CR Generation Rates

08/16/2021

Engineering

Evaluations

03554

DIT-B-03554-00-Provided Program Engineering with

Minimum Allowable Pipe Wall Thicknesses

11/22/2013

Operations Survey Results

06/2019

Miscellaneous

5700-11

Interim Acceptance Criteria for Safety Related Piping System

NDE Reports

1-OHP-4030-102-

017

RCS Pressure Isolation Valves Leak Rate Surveillance Test

10/20/2020

2-EHP-5043-

EDC-001

Evaluation of Degraded/Nonconforming Conditions

29

2-MHP-5021-

2-018

Emergency Diesel Engine Fuel Injector Maintenance

ECP-01

Employee Concerns Program Administration Manual

PMI-7030

Corrective Action Program

PMP-7030-CAP-

001

Action Initiation

PMP-7030-CAP-

2

Condition Action and Closure

PMP-7030-MOP-

001

Corrective Action Program Management Oversight Process

Procedures

PMP-7030-OPR-

Operability Determination

037

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

001

2019-1575-1

GT 2019-1575-1; CRE Program Full SA; ESYN; System

Engineering NSSS

09/25/2019

2019-8560

AR 2019-8560 DIT Inappropriately Updated BOM for SI

Pumps Caused Configuration Change

09/09/2019

2019-8779

ARM-19-09-01 Mods Not Adequately Prepared with Excess

Emergent Problems After Implementation

10/17/2019

21-6317

AR 2021-6317; 1-WRV-723: AB Emergency Diesel North

Combustion Air Aftercooler HE-47-ABN ESW Inlet/Bypass

Valve

07/20/2021

GT 2019-11203

Improvement Actions

11/10/2019

GT 2020-8602

Biennial PI&R Inspection

2/25/2021

NOS 19-04

Material Control, and Measuring and Test Equipment

07/25/2019

NOS-19-03

Maintenance, Work Control, and Special Processes

06/25/2019

NOS-19-05

Nuclear Oversight Audit - Corrective Action Program

07/29/2019

NOS-19-08

NOS Audit - Engineering, Design Control, & In-Service

Inspection (ISI)/In-Service Testing (IST)

10/17/2019

NOS-20-03

NOS Audit NOS-20-03, Emergency Preparedness

04/04/2020

NOS-21-01

REMP/ODCM

04/08/2021

Self-Assessments

SA-2019-ECP-

001

2019 Employee Concerns Annual Assessment

01/17/2020

Work Orders

55547169

Plug Unit 1 NRV-163 and NRV-164 Bellows Tell-Tale at the

Bonnet

11/05/2020