ML22129A205

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Integrated Inspection Report 05000315/2022001 and 05000316/2022001
ML22129A205
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 05/10/2022
From: Nestor Feliz-Adorno
Reactor Projects Region 3 Branch 4
To: Gebbie J
Indiana Michigan Power Co
References
IR 2022001
Download: ML22129A205 (18)


See also: IR 05000315/2022001

Text

May 10, 2022

Mr. Joel P. Gebbie

Senior VP and Chief Nuclear Officer

Indiana Michigan Power Company

Nuclear Generation Group

One Cook Place

Bridgman, MI 49106

SUBJECT: DONALD C. COOK NUCLEAR PLANT - INTEGRATED INSPECTION REPORT

05000315/2022001 AND 05000316/2022001

Dear Mr. Gebbie:

On March 31, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection

at Donald C. Cook Nuclear Plant. On April 13, 2022, the NRC inspectors discussed the results

of this inspection with you and other members of your staff. The results of this inspection are

documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding

involved a violation of NRC requirements. We are treating this violation as a non-cited violation

(NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this

inspection report, you should provide a response within 30 days of the date of this inspection

report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector

at Donald C. Cook Nuclear Plant.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the

NRC Resident Inspector at Donald C. Cook Nuclear Plant.

J. Gebbie 2

This letter, its enclosure, and your response (if any) will be made available for public inspection

and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document

Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public

Inspections, Exemptions, Requests for Withholding.

Sincerely,

Signed by Feliz-Adorno, Nestor

on 05/10/22

Néstor J. Féliz Adorno, Chief

Branch 4

Division of Reactor Projects

Docket Nos. 05000315 and 05000316

License Nos. DPR-58 and DPR-74

Enclosure:

As stated

cc w/ encl: Distribution via LISTSERV

ML22129A205

Non-Sensitive Publicly Available

SUNSI Review

Sensitive Non-Publicly Available

OFFICE RIII RIII

NAME RNg:ve NFélizAdorno

DATE 5/10/2022 5/10/2022

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Numbers: 05000315 and 05000316

License Numbers: DPR-58 and DPR-74

Report Numbers: 05000315/2022001 and 05000316/2022001

Enterprise Identifier: I-2022-001-0060

Licensee: Indiana Michigan Power Company

Facility: Donald C. Cook Nuclear Plant

Location: Bridgman, MI

Inspection Dates: January 01, 2022 to March 31, 2022

Inspectors: B. Daley, Senior Reactor Inspector

T. Iskierka-Boggs, Operations Engineer

J. Mancuso, Senior Resident Inspector

J. Nance, Operations Engineer

R. Ng, Project Engineer

P. Zurawski, Senior Resident Inspector

Approved By: Néstor J. Féliz Adorno, Chief

Branch 4

Division of Reactor Projects

Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an integrated inspection at Donald C. Cook Nuclear Plant, in

accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs

program for overseeing the safe operation of commercial nuclear power reactors. Refer to

https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Fire Zone Separation Not Maintained

Cornerstone Significance Cross-Cutting Report

Aspect Section

Mitigating Green [H.8] - 71111.15

Systems NCV 05000315/2022001-01 Procedure

Open/Closed Adherence

A finding of very low safety significance (Green) and associated non-cited violation (NCV) of

License Condition 2.C(4) was self-revealed for the licensees failure to maintain a 3-hour fire

separation. Specifically, the licensee failed to maintain separation between adjacent fire

zones due to a safety-related fire damper becoming stuck in its damper housing.

Additional Tracking Items

None.

2

PLANT STATUS

Unit 1 began the inspection period at rated thermal power where it remained through the end of

the inspection period. Unit 2 began the inspection period at rated thermal power. On

March 11, 2020, power was reduced to approximately 60 percent for turbine valve testing. The

unit was returned to rated thermal power on March 12, 2022.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed activities described in IMC 2515,

Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of

IPs. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel to assess licensee performance and compliance with Commission rules

and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated readiness for seasonal extreme weather conditions prior to

the onset of extreme cold weather on January 26, 2022.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1) Unit 2 AB Emergency Diesel Generator (EDG) with Unit 2 CD EDG out of service on

January 19, 2022

(2) Unit 2 Control Room Instrumentation Distribution on February 9, 2022

(3) 1CD EDG during 1AB EDG maintenance on February 14, 2022

(4) Unit 2 East Residual Heat Removal (RHR) during West RHR maintenance on

February 15, 2022

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a

walkdown and performing a review to verify program compliance, equipment functionality,

material condition, and operational readiness of the following fire areas:

3

(1) Fire Zone 7: Unit 1 Quadrant 4 Cable Tunnel on January 18, 2022

(2) Fire Zone 8: Unit 1 Quadrant 4 Cable Tunnel on January 18, 2022

(3) Fire Zone 9: Unit 1 Quadrant 3N Cable Tunnel on January 18, 2022

(4) Fire Zone 11: Unit 1 Quadrant 3S Cable Tunnel on January 18, 2022

(5) Fire Zone 64A: Unit 1 North Safety Injection on February 4, 2022

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (1 Sample)

(1) The inspectors reviewed and evaluated the licensed operator examination failure

rates for the requalification annual operating exam and biennial written exam

administered from February 23, 2022 through March 24, 2022.

71111.11B - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Requalification Program (IP Section 03.04) (1 Sample)

(1) Biennial Requalification Written Examinations

The inspectors evaluated the quality of the licensed operator biennial requalification

written examination administered on March 17, 2022.

Annual Requalification Operating Tests

The inspectors evaluated the adequacy of the facility licensees annual requalification

operating test.

Administration of an Annual Requalification Operating Test

The inspectors evaluated the effectiveness of the facility licensee in administering

requalification operating tests required by 10 CFR 55.59(a)(2) and that the facility

licensee is effectively evaluating their licensed operators for mastery of training

objectives.

Requalification Examination Security

The inspectors evaluated the ability of the facility licensee to safeguard examination

material, such that the examination is not compromised.

Remedial Training and Re-examinations

The inspectors evaluated the effectiveness of remedial training conducted by the

licensee, and reviewed the adequacy of re-examinations for licensed operators who

did not pass a required requalification examination.

Operator License Conditions

The inspectors evaluated the licensees program for ensuring that licensed operators

meet the conditions of their licenses.

4

Control Room Simulator

The inspectors evaluated the adequacy of the facility licensees control room

simulator in modeling the actual plant, and for meeting the requirements contained in

10 CFR 55.46.

Problem Identification and Resolution

The inspectors evaluated the licensees ability to identify and resolve problems

associated with licensed operator performance.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)

(1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the Control

Room during Unit 2 Condenser 'A' Waterbox removal from service high risk

operational evolution on February 16, 2022.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated Licensed Operator Requalification

RQ-S-4606-U1-T1 on January 26, 2022.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the

following planned and emergent work activities to ensure configuration changes and

appropriate work controls were addressed:

(1) Maintenance Risk during Unit 2 CD EDG work window on January 24, 2022

(2) Maintenance Risk during Unit 2 RHR work window on February 14, 2022

(3) Maintenance Risk during the March 7 Work Week and High- Risk Switchyard and

Essential Service Water (ESW) work on March 7, 2022

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (7 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the

following operability determinations and functionality assessments:

(1) Action Request (AR) 2022-11514; Elevated Torque on 2-WMO-738 West CCW Heat

Exchanger 2-HE-15W ESW Outlet Valve on January 2, 2022

(2) AR 2022-0512; Manufacturing Defects in Epoxy for 12AB Loop Feed Enclosure on

January 19, 2022

5

(3) AR 2022-0195; 1-HV-ACE-S1-FD Failed to Close; Unit 1 Auxiliary Cable Vault

Ventilation Supply Fire Damper on January 24, 2022

(4) AR 2022-0808; Scaffolding not Built in Accordance with 12-MHP-5021-SCF-001 on

February 2, 2022

(5) AR 2022-1128; Crack in Painted Vent Duct 2-HV-SGRS-8 on February 10, 2022

(6) AR 2022-2250; 2AB EDG Supply Fan Damper Failed on March 28, 2022

(7) AR 2022-2319; Unit 2 Train B CEQ Fan Failed Surveillance Acceptance Criteria on

March 28, 2022

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02)

(1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1) Engineering Change (EC)-54687; Unit 1 Reactor Protection System SPEC200

Refurbishment on March 14, 2022.

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated the following post-maintenance testing activities to verify system

operability and/or functionality:

(1) Unit 1 Stator Cooling Water on January 26, 2022

(2) Unit 2 CD EDG after maintenance on February 3, 2022

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities to verify system operability

and/or functionality:

Surveillance Tests (other) (IP Section 03.01) (3 Samples)

(1) Unit 2 AB EDG on January 25, 2022

(2) Unit 2 Turbine Driven Auxiliary Feedwater Pump on February 11, 2022

(3) Unit 1 Solid State Protection System on February 22, 2022

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated:

(1) Emergency Preparedness (EP) Training Evaluation on January 11, 2022

6

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01) (2 Samples)

(1) Unit 1 (January 1, 2021 through December 31, 2021)

(2) Unit 2 (January 1, 2021 through December 31, 2021)

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02)

(2 Samples)

(1) Unit 1 (January 1, 2021 through December 31, 2021)

(2) Unit 2 (January 1, 2021 through December 31, 2021)

IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (2 Samples)

(1) Unit 1 (January 1, 2021 through December 31, 2021)

(2) Unit 2 (January 1, 2021 through December 31, 2021)

MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04) (2 Samples)

(1) Unit 1 (January 1, 2021 through December 31, 2021)

(2) Unit 2 (January 1, 2021 through December 31, 2021)

INSPECTION RESULTS

Fire Zone Separation Not Maintained

Cornerstone Significance Cross-Cutting Report

Aspect Section

Mitigating Green [H.8] - 71111.15

Systems NCV 05000315/2022001-01 Procedure

Open/Closed Adherence

A finding of very low safety significance (Green) and associated non-cited violation (NCV) of

License Condition 2.C(4) was self-revealed for the licensees failure to maintain a 3-hour fire

separation. Specifically, the licensee failed to maintain separation between adjacent fire

zones due to a safety-related fire damper becoming stuck in its damper housing.

Description:

On January 6, 2022, the safety-related control room auxiliary cable vault supply fan discharge

damper (i.e., 1-HV-ACE-S1-FD) failed to close during a Unit 1 auxiliary cable vault carbon

dioxide (CO2) system actuation. This fire damper was credited by Fire Safety Analysis,

Revision 5, Section 3.1.7, which states Fire Zone 56 and Fire Zone 44-N are separated by

a fire damper assembly having a 3-hour rating. The licensee condition evaluation found

the lower edge of the damper blade was mushroomed to a larger thickness causing the

damper to become lodged in the damper housing when pushed all the way up during

post-test resetting. The damper was routinely tested during CO2 testing (procedure

1-IHP-4030-166-010). This last test was completed on June 30, 2021. With the fire damper

7

stuck in the damper housing, there was no motive (gravity) force on the link to the carbon

dioxide pop-off. The damper did not drop under its own weight because it was mechanically

stuck in its track due to the mushroomed damper blade. The licensee was able to pull the

damper down by applying external force and showed the damper would function if not pushed

all the way up until becoming stuck in the pocket.

Corrective Actions: The licensee took immediate corrective action to repair the damaged

damper blade, performed an operational function test, and restored it to an operable

condition. Additionally, the licensee revised procedure 12-FPP-4030-066-021 to include

inspection for physical damage or deformities to tracks, blades, cables, pop-offs, or fusible

links.

Corrective Action References: AR 2022-0195

Performance Assessment:

Performance Deficiency: The inspectors determined that the licensee's failure to provide a

3-hour fire damper assembly between Fire Zone 56 and Fire Zone 44-N was contrary to the

Fire Safety Analysis and was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Protection Against External Factors attribute of the

Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure

the availability, reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. Specifically, the failure of the damper to fully close resulted in

the unavailability of the fire barrier to prevent a fire to spread between Fire Zone 56 and Fire

Zone 44-N.

Significance: The inspectors assessed the significance of the finding using Appendix F, Fire

Protection and Post - Fire Safe Shutdown SDP. In accordance with Inspection Manual

Chapter 0609, Attachment 0609.04 Initial Characterization of Findings, Table 3 the

inspectors determined the finding affected the Mitigating System cornerstone. The finding

degraded fire protection defense-in-depth strategies, and the inspectors determined that the

finding represented a high degradation. The finding screened as having very low safety

significance (Green) in Step 1.4.4-B of IMC 0609, Appendix F, because there was an

adequate automatic suppression system on either side of the fire confinement element.

Cross-Cutting Aspect: H.8 - Procedure Adherence: Individuals follow processes, procedures,

and work instructions. Specifically, individuals did not follow Attachment 2 of Procedure

1-IHP-4030-166-010, Unit 1 Auxiliary Cable Vault CO2 Fire Suppression Test. This

procedure stated, in part, to only lift the damper as far as required to secure the restraining

link and not push the damper beyond its normal travel range.

Enforcement:

Violation: Donald C. Cook License Condition 2.C(4) states, in part, Indiana Michigan Power

Company shall implement and maintain in effect all provisions of the approved fire protection

program. Fire Safety Analysis, Revision 5, Section 3.1.7 states, in part, Fire Zone 56and Fire

Zone 44-N are separated by a fire damper assembly having a 3-hour rating. Upon closure,

safety-related fire damper 1-HV-ACE-S1-FD fulfilled the required separation between Fire

Zone 56 and 44-N.

Contrary to the above, from June 30, 2021 to January 6, 2022, the licensee failed to maintain

8

in effect all provisions of the approved fire protection program. Specifically, the licensee did

not provide a 3-hour fire damper assembly between Fire Zone 56 and Fire Zone 44-N. While

the licensee installed 3-hour fire damper 1-HV-ACE-S1-FD between these fire zones, the

damper was unable to function as a 3-hour fire barrier because it was mechanically stuck

open.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On April 13, 2022, the inspectors presented the integrated inspection results to

Mr. J. Gebbie, Senior Vice President, and other members of the licensee staff.

On March 18, 2022, the inspectors presented the Biennial Licensed Operator

Requalification program inspection results inspection results to Ms. K. Ferneau, Plant

Manager, and other members of the licensee staff.

On March 29, 2022, the inspectors presented the Licensed Operator Requalification

Program Annual testing summary results inspection results to Mr. T. Kasper, Operations

Training Manager, and other members of the licensee staff.

9

DOCUMENTS REVIEWED

Inspection Type Designation Description or Title Revision or

Procedure Date

71111.01 Procedures PMP-5055-001- Winterization/Summerization 38

001

71111.04 Corrective Action AR 2022-0808 Scaffolding Not Built in Accordance With 0

Documents 12-MHP-5021-SCF-001

AR 2022-1128 Crack in Painted Vent Duct Y at 2-HV-SGRS-8 0

Drawings OP-2-5143 Flow Diagram, Emergency Core Cooling (RHR) 77

Procedures 1-OHL-5030- Unit 1 Tours- Unit 1 Turbine Tour 98

SOM-004

1-OHP-4021-032- DG1CD Operation 050

001cd

1-OHP-4021-032- Operating DG1CD Subsystems 042

008cd

12-MHP-5021- Scaffolding Procedure 39

SCF-001

12-OHP-4021- Operation of the Essential Service Water System 75

019-001

2-OHP-4021-017- Operation of the Residual Hear Removal System 31

001

2-OHP-4021-032- DG2AB Operation 039

001AB

2-OHP-4021-032- Operating DG Subsystems 060

008AB

2-OHP-4021-082- Operation of CRID Power Supplies 043

008

PMP-4043-SLV- Sealed/Locked Valves 72

001

71111.05 Fire Plans Fire Zone 11 Quadrant 3S Cable Tunnel Unit 1 Elev. 596-3.5 41

Fire Zone 64A Safety Injection Pump North Unit 1 Elev. 587-0 41

Fire Zone 7 Quadrant 1 Cable Tunnel Unit 1 Elev. 596-3.5 41

Fire Zone 8 Unit 1 Quadrant 4 Cable Tunnel Unit 1 Elev. 596-3.5 41

Fire Zone 9 Quadrant 3N Cable Tunnel Unit 1 Elev. 596-3.5 41

Miscellaneous Fire Safety D.C. Cook Fire Safety Analysis (FSA) 5

10

Inspection Type Designation Description or Title Revision or

Procedure Date

Analysis

71111.11A Miscellaneous D.C. Cook 2022 Current Cook Licensed Operators 03/29/2022

LOR Annual

Exam Results -

Email dated

3/29/2022 at 8:29

AM from D.C.

Cook Initial

Operations

Training

Supervisor

71111.11B Corrective Action AR 2019-10375 U-1 N HDP Tripped When Removing the M CBP 10/24/2019

Documents AR 2019-10383 Unit 1 North and South Heater Drain Pumps Tripped at 10/23/2019

100% Power

AR 2019-10716 Unit 1 Control Bank D PPC/Control Panel Disagreement 10/31/2019

AR 2019-8732 Unexpected System Response During Main Turbine Valve 09/13/2019

Testing

AR 2020-1416 Operators are Not Consistently Applying Fundamentals 02/11/2020

AR 2020-5707 HELB Door Made Inoperable Without Engineering 07/06/2020

Evaluation

AR 2020-5718 Inoperable HELB Barrier Not Added to Online Risk 07/16/2020

Assessment

AR 2020-6369 Cross Unit Status Control Error 08/09/2020

AR 2020-8488 Unit 2 Reactor Trip - 12 October 2020 10/12/2020

AR 2020-8522 Degraded Vacuum Resulting in Lo SG4 Level 10/12/2020

AR 2021-5671 U-2 SDM Requirements Were Not Procedurally Within Limits 06/04/2021

GT 2020-1496 Training Request for Case Study of 10/23/2019 U1 HDP 02/13/2020

Transient

GT 2021-5700 Training Request on Shutdown Margin (Xenon vs. No 06/25/2021

Xenon)

Drawings OP-1-98509-17 Steam Dumps Control & Turbine Trips Logic Diagram 08/08/2019

Miscellaneous BRE22-C-RO RO Written Examination 02/15/2022

with references

BRE22-C-SRO SRO Written Examination 02/15/2022

11

Inspection Type Designation Description or Title Revision or

Procedure Date

with references

DC Cook Unit 1 Reviewed Multiple Files That Document the Testing of the 09/21/2021

and Unit 2 Unit 1 and Unit 2 Simulators to Proper Operation and Ensure

Simulator Testing They Properly Mimic the Reference Plant

Data

List of Licensed List of Licensed Operators and Medical Conditions 03/03/2022

Operators and

Medical

Conditions

Ops Exam Ops Exam Overlap Document Used to Ensure Overlap 03/03/2022

Overlap Between Weekly LOR Exams Is Adequate

Document

RO-O-E277- Operating Test JPMs - 4 Simulator, 4 In-Plant, 1-RO Admin, 02/01/2022

U12.R2 (SIM); 1-SRO Admin

RO-O-E007B-

U12.R1 (SIM);

RO-O-E276-

U12.R3 (SIM);

RO-O-AEO-

E276.R1

(PLANT);

RO-O-AEO-

E005.R5

(PLANT);

RO-O-AEO-

A006.R3

(PLANT);

RO-O-AEO-

E288.R2

(PLANT);

SR-O-

ADM014.R2

(SRO ADMIN);

RO-O-

12

Inspection Type Designation Description or Title Revision or

Procedure Date

ADM007.R5 (RO

ADMIN);

RO-O-A087-

U12.R1 (SIM)

RQ-E-ANN44; Operating Test Simulator Scenarios 02/01/2022

RQ-E-ANN51;

RQ-E-ANN10;

RQ-E-ANN38

RQ4602-A LOR Period 4602 Exam 06/21/2021

RQ4602-B LOR Period 4402 Exam 05/24/2021

Procedures 1-OHP-5030-050- Main Turbine Trip Testing 12/15/2017

002, Revision 6

12-OHP-2110- Clearance Permit System 11/16/2021

CPS-001

OHI-2071 Reporting Reassignment, Termination, and Conditions 16

Potentially Affecting Performance of Licensed Duties

TRP-2070-TAP- SAT Development 54

300

TRP-2070-TAP- Licensed Operator Requalification Training Annual Operating 8

300-LOR Test and Biennial Written Examination Development

TRP-2070-TAP- Operations Training Examination and Simulator Exercise 23

300-OPS Guide Development

TRP-2070-TAP- SAT Implementation 35

400

TRP-2070-TAP- Licensed Operator Requalification Training Annual Operating 10

400-LOR Test and Biennial Written Examination Implementation

TRP-2070-TAP- Operations Training Implementation 59

400-OPS

TRP-2070-TAP- Operations Training NRC Exam Security 13

400-SEC

Self-Assessments 2021-8546; 2022 Pre-NRC 71111.11 Inspection Quick-Hit 0

Training Self-Assessment

Department

71111.11Q Miscellaneous RQ-S-4606-U1- Licensed Operator Requalification - Period 4606 U1 Training 0

13

Inspection Type Designation Description or Title Revision or

Procedure Date

T1 Scenario 1

Procedures 2-OHP-4021-057- Operation of Main and Feed Pump Condensers 037

006

71111.13 Drawings 12-5967-14 Fire Hazard Analysis Turbine Building Main Floor Elev. 14

633'-0" Units 1 and 2

12-5977-6 Fire Hazard Analysis Reactor Building Main Floor EL. 650'-0" 6

Units 1 and 2

Miscellaneous Unit 1 and 2 Cycle 121, Work Week 10 Risk 0

Unit 1 and 2 Cycle 121, Work Week 07 Risk 0

Unit 1 and 2 Cycle 121, Work Week 04 Risk 0

71111.15 Corrective Action AR 2022-0195 1-HV-ACE-S1-FD failed to close; Unit 1 Auxiliary Cable Vault 0

Documents Ventilation Supply Fire Damper

AR 2022-0512 Manufacturing Defects in Epoxy for 12AB Loop Feed 0

Enclosure

AR 2022-0808 Scaffolding Not Built In Accordance with 0

12-MHP-5021-SCF-001

AR 2022-1128 Crack in Painted Vent Duct 2-HV-SGRS-8 0

AR 2022-1514 Elevated Torque on 2-WMO-738 West CCW Heat 0

Exchanger 2-HE-15W ESW Outlet Valve

AR 2022-2250  ; 2AB EDG Supply Fan Damper Failed 0

AR 2022-2319 Unit 2 Train B CEQ Fan Failed Surveillance Acceptance 0

Criteria

71111.18 Engineering EC-54687 Unit 1 Reactor Protection System SPEC200 Refurbishment 0

Changes

71111.19 Procedures 12-MHP-5021- Emergency Diesel Generator System Mechanical 14

032-146 Maintenance

2-OHP-030-232- CD Diesel Generator Operability Test (Train A) 67

027CD

I-OHP-4021-059- Generator Stator Cooling Water System Operation 32

001

71111.22 Procedures 1-IHP-4030-111- Train B Solid State Protection System (SSPS) Automatic 16

001B Actuation Logic Operational Test (TADOT, Actuation Logic

Test and Master Relay Test) and Reactor Trip Breaker

Operational Test (TADOT)

14

Inspection Type Designation Description or Title Revision or

Procedure Date

1-IHP-4030-111- Train 'B' Solid State Protection System (SSPS) Automatic 016

001B Trip and Actuation Logic Operational Test (TADOT,

Actuation Logic Test, and Master Relay Test) and Reactor

Trip Breaker Operational Test (TADOT)

12-OHP-4021- Racking In and Out Reactor Trip, Reactor Trip Bypass, and 15

082-018 MG Set Output Breakers

2-OHP-4030-232- AB Diesel Generator Operability Test (Train B) 70

027AB

2-OHP-4030-256- Turbine Driven Auxiliary Feedwater System Test 36

017T

2-OHP-4030-256- Turbine Driven Auxiliary Feedwater System Test 36

017T

71114.06 Miscellaneous January 11, 2022 Emergency Planning Drill Scenario 0

71151 Corrective Action AR 2021-1900 Both Units Lost Train B Reserve Feed 02/26/2021

Documents

Miscellaneous Operational Narrative Logs 06/22/2021 -

06/23/2021

Procedures PMP-7110-PIP- Reactor Oversight Program Performance Indicators and 20

001 Monthly Operating Report Data Sheets (January 2021

through December 2021)

15