ML22129A205

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Integrated Inspection Report 05000315/2022001 and 05000316/2022001
ML22129A205
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 05/10/2022
From: Nestor Feliz-Adorno
Reactor Projects Region 3 Branch 4
To: Gebbie J
Indiana Michigan Power Co
References
IR 2022001
Download: ML22129A205 (18)


See also: IR 05000315/2022001

Text

Mr. Joel P. Gebbie

Senior VP and Chief Nuclear Officer

Indiana Michigan Power Company

Nuclear Generation Group

One Cook Place

Bridgman, MI 49106

SUBJECT:

DONALD C. COOK NUCLEAR PLANT - INTEGRATED INSPECTION REPORT

05000315/2022001 AND 05000316/2022001

Dear Mr. Gebbie:

On March 31, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection

at Donald C. Cook Nuclear Plant. On April 13, 2022, the NRC inspectors discussed the results

of this inspection with you and other members of your staff. The results of this inspection are

documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding

involved a violation of NRC requirements. We are treating this violation as a non-cited violation

(NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this

inspection report, you should provide a response within 30 days of the date of this inspection

report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector

at Donald C. Cook Nuclear Plant.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the

NRC Resident Inspector at Donald C. Cook Nuclear Plant.

May 10, 2022

J. Gebbie

2

This letter, its enclosure, and your response (if any) will be made available for public inspection

and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document

Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public

Inspections, Exemptions, Requests for Withholding.

Sincerely,

Néstor J. Féliz Adorno, Chief

Branch 4

Division of Reactor Projects

Docket Nos. 05000315 and 05000316

License Nos. DPR-58 and DPR-74

Enclosure:

As stated

cc w/ encl: Distribution via LISTSERV

Signed by Feliz-Adorno, Nestor

on 05/10/22

ML22129A205

SUNSI Review

Non-Sensitive

Sensitive

Publicly Available

Non-Publicly Available

OFFICE

RIII

RIII

NAME

RNg:ve

NFélizAdorno

DATE

5/10/2022

5/10/2022

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Numbers:

05000315 and 05000316

License Numbers:

DPR-58 and DPR-74

Report Numbers:

05000315/2022001 and 05000316/2022001

Enterprise Identifier:

I-2022-001-0060

Licensee:

Indiana Michigan Power Company

Facility:

Donald C. Cook Nuclear Plant

Location:

Bridgman, MI

Inspection Dates:

January 01, 2022 to March 31, 2022

Inspectors:

B. Daley, Senior Reactor Inspector

T. Iskierka-Boggs, Operations Engineer

J. Mancuso, Senior Resident Inspector

J. Nance, Operations Engineer

R. Ng, Project Engineer

P. Zurawski, Senior Resident Inspector

Approved By:

Néstor J. Féliz Adorno, Chief

Branch 4

Division of Reactor Projects

2

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an integrated inspection at Donald C. Cook Nuclear Plant, in

accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs

program for overseeing the safe operation of commercial nuclear power reactors. Refer to

https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Fire Zone Separation Not Maintained

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000315/2022001-01

Open/Closed

[H.8] -

Procedure

Adherence

71111.15

A finding of very low safety significance (Green) and associated non-cited violation (NCV) of

License Condition 2.C(4) was self-revealed for the licensees failure to maintain a 3-hour fire

separation. Specifically, the licensee failed to maintain separation between adjacent fire

zones due to a safety-related fire damper becoming stuck in its damper housing.

Additional Tracking Items

None.

3

PLANT STATUS

Unit 1 began the inspection period at rated thermal power where it remained through the end of

the inspection period. Unit 2 began the inspection period at rated thermal power. On

March 11, 2020, power was reduced to approximately 60 percent for turbine valve testing. The

unit was returned to rated thermal power on March 12, 2022.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed activities described in IMC 2515,

Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of

IPs. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel to assess licensee performance and compliance with Commission rules

and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated readiness for seasonal extreme weather conditions prior to

the onset of extreme cold weather on January 26, 2022.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1)

Unit 2 AB Emergency Diesel Generator (EDG) with Unit 2 CD EDG out of service on

January 19, 2022

(2)

Unit 2 Control Room Instrumentation Distribution on February 9, 2022

(3)

1CD EDG during 1AB EDG maintenance on February 14, 2022

(4)

Unit 2 East Residual Heat Removal (RHR) during West RHR maintenance on

February 15, 2022

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a

walkdown and performing a review to verify program compliance, equipment functionality,

material condition, and operational readiness of the following fire areas:

4

(1)

Fire Zone 7: Unit 1 Quadrant 4 Cable Tunnel on January 18, 2022

(2)

Fire Zone 8: Unit 1 Quadrant 4 Cable Tunnel on January 18, 2022

(3)

Fire Zone 9: Unit 1 Quadrant 3N Cable Tunnel on January 18, 2022

(4)

Fire Zone 11: Unit 1 Quadrant 3S Cable Tunnel on January 18, 2022

(5)

Fire Zone 64A: Unit 1 North Safety Injection on February 4, 2022

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (1 Sample)

(1)

The inspectors reviewed and evaluated the licensed operator examination failure

rates for the requalification annual operating exam and biennial written exam

administered from February 23, 2022 through March 24, 2022.

71111.11B - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Requalification Program (IP Section 03.04) (1 Sample)

(1)

Biennial Requalification Written Examinations

The inspectors evaluated the quality of the licensed operator biennial requalification

written examination administered on March 17, 2022.

Annual Requalification Operating Tests

The inspectors evaluated the adequacy of the facility licensees annual requalification

operating test.

Administration of an Annual Requalification Operating Test

The inspectors evaluated the effectiveness of the facility licensee in administering

requalification operating tests required by 10 CFR 55.59(a)(2) and that the facility

licensee is effectively evaluating their licensed operators for mastery of training

objectives.

Requalification Examination Security

The inspectors evaluated the ability of the facility licensee to safeguard examination

material, such that the examination is not compromised.

Remedial Training and Re-examinations

The inspectors evaluated the effectiveness of remedial training conducted by the

licensee, and reviewed the adequacy of re-examinations for licensed operators who

did not pass a required requalification examination.

Operator License Conditions

The inspectors evaluated the licensees program for ensuring that licensed operators

meet the conditions of their licenses.

5

Control Room Simulator

The inspectors evaluated the adequacy of the facility licensees control room

simulator in modeling the actual plant, and for meeting the requirements contained in

10 CFR 55.46.

Problem Identification and Resolution

The inspectors evaluated the licensees ability to identify and resolve problems

associated with licensed operator performance.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)

(1 Sample)

(1)

The inspectors observed and evaluated licensed operator performance in the Control

Room during Unit 2 Condenser 'A' Waterbox removal from service high risk

operational evolution on February 16, 2022.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1)

The inspectors observed and evaluated Licensed Operator Requalification

RQ-S-4606-U1-T1 on January 26, 2022.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the

following planned and emergent work activities to ensure configuration changes and

appropriate work controls were addressed:

(1)

Maintenance Risk during Unit 2 CD EDG work window on January 24, 2022

(2)

Maintenance Risk during Unit 2 RHR work window on February 14, 2022

(3)

Maintenance Risk during the March 7 Work Week and High- Risk Switchyard and

Essential Service Water (ESW) work on March 7, 2022

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (7 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the

following operability determinations and functionality assessments:

(1)

Action Request (AR) 2022-11514; Elevated Torque on 2-WMO-738 West CCW Heat

Exchanger 2-HE-15W ESW Outlet Valve on January 2, 2022

(2)

AR 2022-0512; Manufacturing Defects in Epoxy for 12AB Loop Feed Enclosure on

January 19, 2022

6

(3)

AR 2022-0195; 1-HV-ACE-S1-FD Failed to Close; Unit 1 Auxiliary Cable Vault

Ventilation Supply Fire Damper on January 24, 2022

(4)

AR 2022-0808; Scaffolding not Built in Accordance with 12-MHP-5021-SCF-001 on

February 2, 2022

(5)

AR 2022-1128; Crack in Painted Vent Duct 2-HV-SGRS-8 on February 10, 2022

(6)

AR 2022-2250; 2AB EDG Supply Fan Damper Failed on March 28, 2022

(7)

AR 2022-2319; Unit 2 Train B CEQ Fan Failed Surveillance Acceptance Criteria on

March 28, 2022

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02)

(1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1)

Engineering Change (EC)-54687; Unit 1 Reactor Protection System SPEC200

Refurbishment on March 14, 2022.

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated the following post-maintenance testing activities to verify system

operability and/or functionality:

(1)

Unit 1 Stator Cooling Water on January 26, 2022

(2)

Unit 2 CD EDG after maintenance on February 3, 2022

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities to verify system operability

and/or functionality:

Surveillance Tests (other) (IP Section 03.01) (3 Samples)

(1)

Unit 2 AB EDG on January 25, 2022

(2)

Unit 2 Turbine Driven Auxiliary Feedwater Pump on February 11, 2022

(3)

Unit 1 Solid State Protection System on February 22, 2022

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated:

(1)

Emergency Preparedness (EP) Training Evaluation on January 11, 2022

7

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01) (2 Samples)

(1)

Unit 1 (January 1, 2021 through December 31, 2021)

(2)

Unit 2 (January 1, 2021 through December 31, 2021)

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02)

(2 Samples)

(1)

Unit 1 (January 1, 2021 through December 31, 2021)

(2)

Unit 2 (January 1, 2021 through December 31, 2021)

IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (2 Samples)

(1)

Unit 1 (January 1, 2021 through December 31, 2021)

(2)

Unit 2 (January 1, 2021 through December 31, 2021)

MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04) (2 Samples)

(1)

Unit 1 (January 1, 2021 through December 31, 2021)

(2)

Unit 2 (January 1, 2021 through December 31, 2021)

INSPECTION RESULTS

Fire Zone Separation Not Maintained

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000315/2022001-01

Open/Closed

[H.8] -

Procedure

Adherence

71111.15

A finding of very low safety significance (Green) and associated non-cited violation (NCV) of

License Condition 2.C(4) was self-revealed for the licensees failure to maintain a 3-hour fire

separation. Specifically, the licensee failed to maintain separation between adjacent fire

zones due to a safety-related fire damper becoming stuck in its damper housing.

Description:

On January 6, 2022, the safety-related control room auxiliary cable vault supply fan discharge

damper (i.e., 1-HV-ACE-S1-FD) failed to close during a Unit 1 auxiliary cable vault carbon

dioxide (CO2) system actuation. This fire damper was credited by Fire Safety Analysis,

Revision 5, Section 3.1.7, which states Fire Zone 56 and Fire Zone 44-N are separated by

a fire damper assembly having a 3-hour rating. The licensee condition evaluation found

the lower edge of the damper blade was mushroomed to a larger thickness causing the

damper to become lodged in the damper housing when pushed all the way up during

post-test resetting. The damper was routinely tested during CO2 testing (procedure

1-IHP-4030-166-010). This last test was completed on June 30, 2021. With the fire damper

8

stuck in the damper housing, there was no motive (gravity) force on the link to the carbon

dioxide pop-off. The damper did not drop under its own weight because it was mechanically

stuck in its track due to the mushroomed damper blade. The licensee was able to pull the

damper down by applying external force and showed the damper would function if not pushed

all the way up until becoming stuck in the pocket.

Corrective Actions: The licensee took immediate corrective action to repair the damaged

damper blade, performed an operational function test, and restored it to an operable

condition. Additionally, the licensee revised procedure 12-FPP-4030-066-021 to include

inspection for physical damage or deformities to tracks, blades, cables, pop-offs, or fusible

links.

Corrective Action References: AR 2022-0195

Performance Assessment:

Performance Deficiency: The inspectors determined that the licensee's failure to provide a

3-hour fire damper assembly between Fire Zone 56 and Fire Zone 44-N was contrary to the

Fire Safety Analysis and was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Protection Against External Factors attribute of the

Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure

the availability, reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. Specifically, the failure of the damper to fully close resulted in

the unavailability of the fire barrier to prevent a fire to spread between Fire Zone 56 and Fire

Zone 44-N.

Significance: The inspectors assessed the significance of the finding using Appendix F, Fire

Protection and Post - Fire Safe Shutdown SDP. In accordance with Inspection Manual

Chapter 0609, Attachment 0609.04 Initial Characterization of Findings, Table 3 the

inspectors determined the finding affected the Mitigating System cornerstone. The finding

degraded fire protection defense-in-depth strategies, and the inspectors determined that the

finding represented a high degradation. The finding screened as having very low safety

significance (Green) in Step 1.4.4-B of IMC 0609, Appendix F, because there was an

adequate automatic suppression system on either side of the fire confinement element.

Cross-Cutting Aspect: H.8 - Procedure Adherence: Individuals follow processes, procedures,

and work instructions. Specifically, individuals did not follow Attachment 2 of Procedure

1-IHP-4030-166-010, Unit 1 Auxiliary Cable Vault CO2 Fire Suppression Test. This

procedure stated, in part, to only lift the damper as far as required to secure the restraining

link and not push the damper beyond its normal travel range.

Enforcement:

Violation: Donald C. Cook License Condition 2.C(4) states, in part, Indiana Michigan Power

Company shall implement and maintain in effect all provisions of the approved fire protection

program. Fire Safety Analysis, Revision 5, Section 3.1.7 states, in part, Fire Zone 56and Fire

Zone 44-N are separated by a fire damper assembly having a 3-hour rating. Upon closure,

safety-related fire damper 1-HV-ACE-S1-FD fulfilled the required separation between Fire

Zone 56 and 44-N.

Contrary to the above, from June 30, 2021 to January 6, 2022, the licensee failed to maintain

9

in effect all provisions of the approved fire protection program. Specifically, the licensee did

not provide a 3-hour fire damper assembly between Fire Zone 56 and Fire Zone 44-N. While

the licensee installed 3-hour fire damper 1-HV-ACE-S1-FD between these fire zones, the

damper was unable to function as a 3-hour fire barrier because it was mechanically stuck

open.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On April 13, 2022, the inspectors presented the integrated inspection results to

Mr. J. Gebbie, Senior Vice President, and other members of the licensee staff.

On March 18, 2022, the inspectors presented the Biennial Licensed Operator

Requalification program inspection results inspection results to Ms. K. Ferneau, Plant

Manager, and other members of the licensee staff.

On March 29, 2022, the inspectors presented the Licensed Operator Requalification

Program Annual testing summary results inspection results to Mr. T. Kasper, Operations

Training Manager, and other members of the licensee staff.

10

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.01

Procedures

PMP-5055-001-

001

Winterization/Summerization

38

AR 2022-0808

Scaffolding Not Built in Accordance With

12-MHP-5021-SCF-001

0

Corrective Action

Documents

AR 2022-1128

Crack in Painted Vent Duct Y at 2-HV-SGRS-8

0

Drawings

OP-2-5143

Flow Diagram, Emergency Core Cooling (RHR)

77

1-OHL-5030-

SOM-004

Unit 1 Tours- Unit 1 Turbine Tour

98

1-OHP-4021-032-

001cd

DG1CD Operation

050

1-OHP-4021-032-

008cd

Operating DG1CD Subsystems

042

12-MHP-5021-

SCF-001

Scaffolding Procedure

39

12-OHP-4021-

019-001

Operation of the Essential Service Water System

75

2-OHP-4021-017-

001

Operation of the Residual Hear Removal System

31

2-OHP-4021-032-

001AB

DG2AB Operation

039

2-OHP-4021-032-

008AB

Operating DG Subsystems

060

2-OHP-4021-082-

008

Operation of CRID Power Supplies

043

71111.04

Procedures

PMP-4043-SLV-

001

Sealed/Locked Valves

72

Fire Zone 11

Quadrant 3S Cable Tunnel Unit 1 Elev. 596-3.5

41

Fire Zone 64A

Safety Injection Pump North Unit 1 Elev. 587-0

41

Fire Zone 7

Quadrant 1 Cable Tunnel Unit 1 Elev. 596-3.5

41

Fire Zone 8

Unit 1 Quadrant 4 Cable Tunnel Unit 1 Elev. 596-3.5

41

Fire Plans

Fire Zone 9

Quadrant 3N Cable Tunnel Unit 1 Elev. 596-3.5

41

71111.05

Miscellaneous

Fire Safety

D.C. Cook Fire Safety Analysis (FSA)

5

11

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Analysis

71111.11A

Miscellaneous

D.C. Cook 2022

LOR Annual

Exam Results -

Email dated

3/29/2022 at 8:29

AM from D.C.

Cook Initial

Operations

Training

Supervisor

Current Cook Licensed Operators

03/29/2022

AR 2019-10375

U-1 N HDP Tripped When Removing the M CBP

10/24/2019

AR 2019-10383

Unit 1 North and South Heater Drain Pumps Tripped at

100% Power

10/23/2019

AR 2019-10716

Unit 1 Control Bank D PPC/Control Panel Disagreement

10/31/2019

AR 2019-8732

Unexpected System Response During Main Turbine Valve

Testing

09/13/2019

AR 2020-1416

Operators are Not Consistently Applying Fundamentals

02/11/2020

AR 2020-5707

HELB Door Made Inoperable Without Engineering

Evaluation

07/06/2020

AR 2020-5718

Inoperable HELB Barrier Not Added to Online Risk

Assessment

07/16/2020

AR 2020-6369

Cross Unit Status Control Error

08/09/2020

AR 2020-8488

Unit 2 Reactor Trip - 12 October 2020

10/12/2020

AR 2020-8522

Degraded Vacuum Resulting in Lo SG4 Level

10/12/2020

AR 2021-5671

U-2 SDM Requirements Were Not Procedurally Within Limits

06/04/2021

GT 2020-1496

Training Request for Case Study of 10/23/2019 U1 HDP

Transient

02/13/2020

Corrective Action

Documents

GT 2021-5700

Training Request on Shutdown Margin (Xenon vs. No

Xenon)

06/25/2021

Drawings

OP-1-98509-17

Steam Dumps Control & Turbine Trips Logic Diagram

08/08/2019

BRE22-C-RO

with references

RO Written Examination

02/15/2022

71111.11B

Miscellaneous

BRE22-C-SRO

SRO Written Examination

02/15/2022

12

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

with references

DC Cook Unit 1

and Unit 2

Simulator Testing

Data

Reviewed Multiple Files That Document the Testing of the

Unit 1 and Unit 2 Simulators to Proper Operation and Ensure

They Properly Mimic the Reference Plant

09/21/2021

List of Licensed

Operators and

Medical

Conditions

List of Licensed Operators and Medical Conditions

03/03/2022

Ops Exam

Overlap

Document

Ops Exam Overlap Document Used to Ensure Overlap

Between Weekly LOR Exams Is Adequate

03/03/2022

RO-O-E277-

U12.R2 (SIM);

RO-O-E007B-

U12.R1 (SIM);

RO-O-E276-

U12.R3 (SIM);

RO-O-AEO-

E276.R1

(PLANT);

RO-O-AEO-

E005.R5

(PLANT);

RO-O-AEO-

A006.R3

(PLANT);

RO-O-AEO-

E288.R2

(PLANT);

SR-O-

ADM014.R2

(SRO ADMIN);

RO-O-

Operating Test JPMs - 4 Simulator, 4 In-Plant, 1-RO Admin,

1-SRO Admin

02/01/2022

13

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

ADM007.R5 (RO

ADMIN);

RO-O-A087-

U12.R1 (SIM)

RQ-E-ANN44;

RQ-E-ANN51;

RQ-E-ANN10;

RQ-E-ANN38

Operating Test Simulator Scenarios

02/01/2022

RQ4602-A

LOR Period 4602 Exam

06/21/2021

RQ4602-B

LOR Period 4402 Exam

05/24/2021

1-OHP-5030-050-

002, Revision 6

Main Turbine Trip Testing

12/15/2017

12-OHP-2110-

CPS-001

Clearance Permit System

11/16/2021

OHI-2071

Reporting Reassignment, Termination, and Conditions

Potentially Affecting Performance of Licensed Duties

16

TRP-2070-TAP-

300

SAT Development

54

TRP-2070-TAP-

300-LOR

Licensed Operator Requalification Training Annual Operating

Test and Biennial Written Examination Development

8

TRP-2070-TAP-

300-OPS

Operations Training Examination and Simulator Exercise

Guide Development

23

TRP-2070-TAP-

400

SAT Implementation

35

TRP-2070-TAP-

400-LOR

Licensed Operator Requalification Training Annual Operating

Test and Biennial Written Examination Implementation

10

TRP-2070-TAP-

400-OPS

Operations Training Implementation

59

Procedures

TRP-2070-TAP-

400-SEC

Operations Training NRC Exam Security

13

Self-Assessments 2021-8546;

Training

Department

2022 Pre-NRC 71111.11 Inspection Quick-Hit

Self-Assessment

0

71111.11Q

Miscellaneous

RQ-S-4606-U1-

Licensed Operator Requalification - Period 4606 U1 Training

0

14

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

T1

Scenario 1

Procedures

2-OHP-4021-057-

006

Operation of Main and Feed Pump Condensers

037

12-5967-14

Fire Hazard Analysis Turbine Building Main Floor Elev.

633'-0" Units 1 and 2

14

Drawings

12-5977-6

Fire Hazard Analysis Reactor Building Main Floor EL. 650'-0"

Units 1 and 2

6

Unit 1 and 2 Cycle 121, Work Week 10 Risk

0

Unit 1 and 2 Cycle 121, Work Week 07 Risk

0

71111.13

Miscellaneous

Unit 1 and 2 Cycle 121, Work Week 04 Risk

0

AR 2022-0195

1-HV-ACE-S1-FD failed to close; Unit 1 Auxiliary Cable Vault

Ventilation Supply Fire Damper

0

AR 2022-0512

Manufacturing Defects in Epoxy for 12AB Loop Feed

Enclosure

0

AR 2022-0808

Scaffolding Not Built In Accordance with

12-MHP-5021-SCF-001

0

AR 2022-1128

Crack in Painted Vent Duct 2-HV-SGRS-8

0

AR 2022-1514

Elevated Torque on 2-WMO-738 West CCW Heat

Exchanger 2-HE-15W ESW Outlet Valve

0

AR 2022-2250

2AB EDG Supply Fan Damper Failed

0

71111.15

Corrective Action

Documents

AR 2022-2319

Unit 2 Train B CEQ Fan Failed Surveillance Acceptance

Criteria

0

71111.18

Engineering

Changes

EC-54687

Unit 1 Reactor Protection System SPEC200 Refurbishment

0

12-MHP-5021-

032-146

Emergency Diesel Generator System Mechanical

Maintenance

14

2-OHP-030-232-

027CD

CD Diesel Generator Operability Test (Train A)

67

71111.19

Procedures

I-OHP-4021-059-

001

Generator Stator Cooling Water System Operation

32

71111.22

Procedures

1-IHP-4030-111-

001B

Train B Solid State Protection System (SSPS) Automatic

Actuation Logic Operational Test (TADOT, Actuation Logic

Test and Master Relay Test) and Reactor Trip Breaker

Operational Test (TADOT)

16

15

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

1-IHP-4030-111-

001B

Train 'B' Solid State Protection System (SSPS) Automatic Trip and Actuation Logic Operational Test (TADOT,

Actuation Logic Test, and Master Relay Test) and Reactor

Trip Breaker Operational Test (TADOT)

016

12-OHP-4021-

082-018

Racking In and Out Reactor Trip, Reactor Trip Bypass, and

MG Set Output Breakers

15

2-OHP-4030-232-

027AB

AB Diesel Generator Operability Test (Train B)

70

2-OHP-4030-256-

017T

Turbine Driven Auxiliary Feedwater System Test

36

2-OHP-4030-256-

017T

Turbine Driven Auxiliary Feedwater System Test

36

71114.06

Miscellaneous

January 11, 2022 Emergency Planning Drill Scenario

0

Corrective Action

Documents

AR 2021-1900

Both Units Lost Train B Reserve Feed

02/26/2021

Miscellaneous

Operational Narrative Logs

06/22/2021 -

06/23/2021

71151

Procedures

PMP-7110-PIP-

001

Reactor Oversight Program Performance Indicators and

Monthly Operating Report Data Sheets (January 2021

through December 2021)

20