IR 05000458/2018003

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NRC Integrated Inspection Report 05000458/2018003
ML18313A028
Person / Time
Site: River Bend Entergy icon.png
Issue date: 11/08/2018
From: Jason Kozal
NRC/RGN-IV/DRP
To: Maguire W
Entergy Operations
References
IR 2018003
Download: ML18313A028 (24)


Text

November 8, 2018

SUBJECT:

RIVER BEND STATION - NRC INTEGRATED INSPECTION REPORT 05000458/2018003

Dear Mr. Maguire:

On September 30, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your River Bend Station, Unit 1. On October 18, 2018, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

No NRC-identified or self-revealing findings were identified during this inspection. However, inspectors documented a licensee-identified violation which was determined to be of very low safety significance in this report. The NRC is treating this violation as a non-cited violation consistent with Section 2.3.2.a of the NRC Enforcement Policy.

If you contest the violation or significance of the non-cited violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC resident inspector at the River Bend Station. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA David Proulx Acting for/

Jason W. Kozal, Chief Project Branch C Division of Reactor Projects

Docket No. 50-458 License No. NPF-47

Enclosure:

Inspection Report 05000458/2018003 w/ Attachment: Documents Reviewed

Enclosure U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Number(s):

05000458

License Number(s):

NPF-47

Report Number(s):

05000458/2018003

Enterprise Identifier: I-2018-003-0009

Licensee:

Entergy Operations, Inc.

Facility:

River Bend Station

Location:

Saint Francisville, Louisiana

Inspection Dates:

July 1, 2018 to September 30, 2018

Inspectors:

J. Sowa, Senior Resident Inspector

C. Speer, Acting Senior Resident Inspector

B. Parks, Resident Inspector

P. Elkmann, Senior Emergency Preparedness Inspector

G. Pick, Senior Reactor Inspector

H. Freeman, Senior Reactor Inspector

R. Kopriva, Senior Reactor Inspector

C. Stott, Reactor Inspector

S. Makor, Reactor Inspector

C. Osterholtz, Senior Operations Engineer

N. Hernandez, Operations Engineer

M. Chambers, Security Specialist

Approved By:

J. Kozal, Chief,

Project Branch C

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at River Bend Station in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC-identified and self-revealed findings, violations, and additional items are summarized in the table below.

Licensee-identified non-cited violations are documented in the Inspection Results at the end of this report.

No findings or violations of more than minor significance were identified during the inspection.

Additional Tracking Items

Type Issue number Title Inspection Procedure Status LER 05000458/2017-004-01 Loss of High Pressure Core Spray Safety Function During Surveillance Due to Malfunction of Test Return Valve 71153 Closed LER 05000458/2018-001-00 Potential Loss of Safety Function of Control Building HVAC Due to Legacy Design Flaw 71153 Closed LER 05000458/2018-004-00 Unanalyzed Condition Due to Inappropriate Protection from Tornado Generated Missiles 71153 Closed VIO 05000458/2017009-01 Failure to Obtain Prior NRC Approval for a Change in Reactor Core Isolation Cooling Injection Point 92702 Closed

PLANT STATUS

River Bend Station began the inspection period at rated thermal power. On August 14, 2018, the unit was down powered to 70 percent in order to troubleshoot a failed pilot solenoid associated with a main steam isolation valve and to conduct power suppression testing. The unit was returned to rated thermal power on August 30, 2018. On September 21, 2018, the unit was down powered to 60 percent for a control rod sequence exchange and to suppress a suspected nuclear fuel leak. The unit was returned to rated thermal power on September 28, 2018, and remained at or near rated thermal power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01Adverse Weather Protection External Flooding

The inspectors evaluated readiness to cope with external flooding on July 18, 2018.

71111.04Equipment Alignment Partial Walkdown

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Residual heat removal A system on July 5, 2018
(2) Residual heat removal C system on July 18, 2018
(3) Reactor core isolation cooling system on July 18, 2018

Complete Walkdown (1 Sample)

The inspectors evaluated system configurations during a complete walkdown of the Division I and Division II standby liquid control systems on July 23, 2018.

71111.05AQFire Protection Annual/Quarterly Quarterly Inspection

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Residual heat removal pump A room, fire area AB-5, on July 5, 2018
(2) Residual heat removal pump C room, fire area AB-4/Z-1 and Z-2, on July 18, 2018
(3) Reactor core isolation cooling pump room, fire area AB-4/Z-1 and Z-2, on July 18, 2018
(4) Standby liquid control area, fire area RC-4/Z-4, on July 23, 2018

71111.06Flood Protection Measures Internal Flooding

The inspectors evaluated internal flooding mitigation protections in residual heat removal pump room B on September 4, 2018.

71111.07Heat Sink Performance Heat Sink

The inspectors evaluated residual heat removal B heat exchanger performance on September 26, 2018.

71111.11Licensed Operator Requalification Program and Licensed Operator Performance Operator Requalification

The inspectors observed and evaluated a portion of an annual requalification test for licensed operators on August 16, 2018.

Operator Performance (1 Sample)

The inspectors observed and evaluated the operators performance during a period of heightened risk associated with reactor power maneuvering following a rod pattern adjustment on August 30, 2018.

Operator Exams (1 Sample)

The inspectors reviewed and evaluated requalification examination results on September 21, 2018.

Operator Requalification Program (1 Sample)

The inspectors evaluated the operator requalification program from August 27, 2018, to September 21, 2018.

71111.12Maintenance Effectiveness Routine Maintenance Effectiveness

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) Functional failure review of the residual heat removal system on September 19, 2018

Quality Control (1 Sample)

The inspectors evaluated maintenance and quality control activities associated with the following equipment performance issues:

(1) Work order for emergency diesel generator relay (EGS-PNL3A-R2) replacement missing safety class and seismic qualification information on July 17, 2018

71111.13Maintenance Risk Assessments and Emergent Work Control

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Yellow risk during extended maintenance outage on Division II diesel generator on July 2, 2018
(2) Yellow shutdown risk condition with reactor core isolation cooling out of service for testing on July 10, 2018
(3) Yellow risk during discharge check valve replacement on Division I standby service water system on July 30, 2018

71111.15Operability Determinations and Functionality Assessments

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Division II standby service water normal service water return valve SWP-MOV96B could not be opened remotely on July 11, 2018
(2) Primary containment following alarm in annulus radiation detector on July 25, 2018
(3) Main steam isolation valve B21-F022B following loss of electrical power to the B solenoid for B21-AOVF022B on August 27, 2018

71111.17TEvaluations of Changes, Tests and Experiments

The inspectors evaluated the following from September 10 to September 14, 2018:

10 CFR 50.59 Evaluations

(1) EC No. 54958 - Install a modern digital turbine control system (Westinghouse Ovation) to replace the current analog C85 steam bypass and pressure control system and the Mark II turbine control system.
(2) EN-2017-002 - While running the Division I emergency diesel generator for a scheduled test, a water leak was found on the jacket water system exhaust jacket behind the number 6 cylinder. The Process Applicability Determination (PAD)determined that the manual operator action to implement the compensatory measures should be evaluated under 10 CFR 50.59.
(3) EN-2015-001 - Core operating limit report for updated fuel loading pattern for Cycles C19A, C19B, and C19C due to leaking fuel bundles.
(4) EN-2015-003 - Updated methodology for calculating ultimate heat sink heat load to determine ultimate heat sink minimum technical specification level.
(5) EN-2017-001 - Core operating limit report for updated fuel loading pattern for Cycle C20A due to leaking fuel bundles.
(6) EN-2015-004 - The design Release Time of the affected Agastat relays, the main steam isolation valve closure/reactor protection system trip circuits could exceed their technical requirements manual response time values even if all relays in the circuit operated within their design specifications and this specific condition is limited to 4 of the 16 loops associated with the main steam isolation valve closure scram circuits.

The design and licensing basis proposed change provides an upper limit for the scram delay time to bind the design of the Agastat relays.

(7) EN-2016-001 - EC 59951 implements a design to provide an alternate method of ensuring that the reactor feedwater pumps are tripped on increasing reactor pressure vessel level during a fire in the main control room that prevents the plant operators from securing the feedwater system in the normal manner.

10 CFR 50.59 Screening/Applicability Determinations

(1) PAD EC-58840 - Condition Report CR-RBS-2014-02754 documents failures during the performance of Surveillance Test Procedures STP-508-4812 and STP-508-4813.

The response time in Step 7.5.11 was found to be 102 milliseconds for the A channel and 94 milliseconds for the B channel, which exceed the technical requirements manual limit of 90 milliseconds.

(2) PAD EC-56521 - The temporary modification installed a gag on residual heat removal heat exchanger cooling water relief valve E12-RVF100B and credited locked open manual valve E12-VF014B to prevent a thermal overpressure condition in the piping between E12-VF014B and E12-MOVF068B.
(3) PAD EC-53558 - Replacement of Gould J series relays with Allen Bradley relays.
(4) PAD EC-16264 - Replace the existing General Electric supplied series 6823 heater controllers manufactured by Electronic Control Systems, with new digital controllers supplied by OMEGA model number CNI8DH44.
(5) PAD EC-76398 - Provide acceptable replacement relays for existing safety-related Gould J11 Series, 120 VAC, permanent magnet latching relays with a relay assembly comprised of an Allen Bradley base relay 700-P400A1 with a latching attachment 700-PLL11A1 as a replacement.
(6) PAD EC-68298 - To temporarily swap the storage locations for the steam dryer and the steam separator to expedite refueling activities.
(7) PAD EC-49287 - Service water check valves SWP-V199 and SWP-V200 internals removal.
(8) PAD EC-57658 - Raise ultimate heat sink level alarm setpoints to allow maximum inventory.
(9) PAD EC-59110 - Upgrade and relocate positioners for reactor feedwater level control valves C33-LVF001A/B/C and reactor feedwater startup valve C33-LVF002.
(10) PAD EC-67339 - Reactor water cleanup regenerative heat exchanger permanent shielding installation.
(11) PAD EC-67341 - Reactor water cleanup non-regenerative heat exchanger permanent shielding installation.
(12) PAD EC-72603 - Standby diesel generator exhaust pipe manifold modification to address exhaust piping flange bolt failures.
(13) PAD LBDCR-2016-02 - Correction to Technical Requirement Manual 3.6.1.2 to delete requirement to test airlock before each restart.
(14) PAD EC-55881 - Revises ultimate heat sink basin minimum technical specification level increase and ultimate heat sink heat load calculation.
(15) PAD EC-60680 - Issues a new calculation G13.18.3.6*027, required to calculate the voltages for the subject motor operated valves during a high energy line break scenario analyzing at relay dropout rather than relay reset.
(16) PAD EC-63133 - Proposes to modify six existing Masterpact circuit breakers associated with Class 1E switchgear EJS-SWG1A, EJS-SWG1B, EJS-SWG2A, and EJS-SWG2B by placing a normally closed contact in series with each breaker-closing coil.
(17) PAD EC-64630 - The proposed activity provides a document change that revises River Bend Station Design Criterion 240.201A, Post-Fire Safe Shutdown
Analysis.
(18) PAD EC-64657 - This engineering change replaces the voltage regulator and part of the control circuitry for reactor protection system motor generator set C71-S001A and C71-S001B.
(19) PAD EC65450 - This modification updates the capacity factor calculation (G13.18.9.0-008 Estimate of River Bend Station Capacity Factor for Environmental Qualification Applications) and updates the cable environmental qualification assessment reports to reflect the changed normal dose impact on the environmental qualification replacement frequency.

71111.19Post Maintenance Testing

The inspectors evaluated the following post maintenance tests:

(1) STP-309-0207, Revision 27, Division II Diesel Generator 184 Day Operability Test, following extended maintenance outage on Division II emergency diesel generator on July 3, 2018
(2) STP-204-6302, Revision 33, Division II LPCI Pump and Valve Operability Test, post-maintenance test following maintenance on residual heat removal C line fill pump check valve E12-VF084C on July 28, 2018
(3) EN-WM-105, Revision 21, Mechanical Maintenance Test: Valve, Glove or Gate, post-maintenance test following replacement of residual heat removal C pump suction vent valve E12-VF013C on August 2, 2018
(4) STP-209-6310, Revision 40, RCIC Quarterly Pump and Valve Operability Test, following replacement of remote servo mechanism in reactor core isolation cooling system on August 14, 2018

===71111.22Surveillance Testing The inspectors evaluated the following surveillance tests:

Routine===

(1) STP-207-4539, Revision 301, RCIC Isolation - RCIC Steam Supply Pressure - Low Channel Functional Test, on August 9, 2018
(2) STP-204-6301, Revision 28, Div I LPCI (RHR) Pump and Valve Operability Test, on August 28, 2018

71114.01Exercise Evaluation

The inspectors evaluated the biennial emergency plan exercise conducted on June 27, 2018. The exercise scenario simulated the inability to secure a liquid radioactive release above discharge permit limits, a catastrophic jet pump failure in the reactor which created fragments which damaged reactor fuel, failure of the reactor protection system to shut down the reactor, failures of the reactor core isolation cooling and high pressure core spray systems, a leak in the reactor water cleanup system outside of containment, and a monitored release through turbine building ventilation. The inspectors discussed the exercise with staff at FEMA Region VI.

71114.04Emergency Action Level and Emergency Plan Changes

The inspectors evaluated submitted River Bend Station On-Shift Staffing Analysis Final Report, Revision 1, dated November 14, 2017, on July 3, 2018. This evaluation does not constitute NRC approval.

71114.06Drill Evaluation Drill/Training Evolution

The inspectors evaluated a site-wide emergency preparedness drill on September 25, 2018.

71114.08Exercise Evaluation - Scenario Review

The inspectors reviewed and evaluated the proposed scenario for biennial emergency plan exercise on May 22, 2018. This review does not constitute NRC approval. The inspectors discussed the proposed scenario with staff at FEMA Region VI.

OTHER ACTIVITIES - BASELINE

71151Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

(1) MS08: Heat Removal Systems (07/01/2017-06/30/2018)
(2) MS09: Residual Heat Removal Systems (07/01/2017-06/30/2018)
(3) MS10: Cooling Water Support Systems (07/01/2017-06/30/2018)
(4) EP01: Drill/Exercise Performance Sample (04/01/2017-03/31/2018)
(5) EP02: Emergency Response Organization Drill Participation Sample (04/01/2017-03/31/2018)
(6) EP03: Alert And Notification System Reliability Sample (04/01/2017-03/31/2018)

71153Follow-up of Events and Notices of Enforcement Discretion Licensee Event Reports

The inspectors evaluated the following licensee event reports (LERs) which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:

(1) LER 05000458/2017-004-01, Loss of High Pressure Core Spray Safety Function During Surveillance Due to Malfunction of Test Return Valve on March 23, 2017.

The inspectors reviewed the updated LER submittal and did not identify any additional performance deficiencies. The previous LER submittal was reviewed in Inspection Report 05000458/2017004.

(2) LER 05000458/2018-001-00, Potential Loss of Safety Function of Control Building HVAC Due to Legacy Design Flaw on September 18, 2018.

The inspectors reviewed this LER and documented a licensee-identified violation.

(3) LER 05000458/2018-004-00, Unanalyzed Condition Due to Inappropriate Protection from Tornado Generated Missiles on May 4, 2018

The inspectors reviewed this LER and did not identify any performance deficiencies.

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL 92702Follow-up on Traditional Enforcement Actions Including Violations, Deviations, Confirmatory Action Letters, Confirmatory Orders, and Alternative Dispute Resolution Confirmatory Orders The inspectors reviewed the licensees response to Notice of Violation 05000458/2017009-01 and determined that the reason, corrective actions taken and planned to address recurrence, and the date when full compliance will be achieved for this violation are adequately addressed and captured on the docket.

INSPECTION RESULTS

Licensee-Identified Non-Cited Violation 71153 - Follow-up of Events and Notices of Enforcement Discretion This violation of very low safety significance was identified by the licensee and has been entered into the licensee corrective action program and is being treated as a non-cited violation, consistent with Section 2.3.2.a of the NRC Enforcement Policy.

Violation: Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part, that measures shall be established to assure that the design basis for those structures, systems, and components to which Appendix B applies is correctly translated into specifications, drawings, procedures, and instructions. The design basis for the control building air conditioning system, as specified in the updated safety analysis report, requires that the system be capable of performing its safety function in the event of a single failure in any component.

Contrary to the above, the licensee failed to assure that the design basis was correctly translated into specifications for the control building air conditioning system. Specifically, while reviewing the control logic for the control building air conditioning system, the licensee discovered that the control logic was designed such that a single failure in a component in the control logic could have prevented the system from performing its specified safety function.

Significance/Severity Level: The inspectors determined that the finding was of very low safety significance (Green) because it did not represent an actual loss of function of at least a single train for greater than its technical specification outage time and it did not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety significance in accordance with the licensees Maintenance Rule program for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Corrective Action Reference(s): CR-RBS-2018-02211

EXIT MEETINGS AND DEBRIEFS

On May 21, 2018, the inspectors discussed the proposed biennial exercise scenario with Ms. D. Bordelon, Branch Chief, Technological Hazards Branch, FEMA Region VI.

On May 22, 2018, the inspectors discussed the proposed biennial exercise scenario with Mr. R. Leasure, Manager, Emergency Preparedness, and other members of the licensee staff.

On May 28, 2018, the inspectors discussed the biennial emergency plan exercise conducted June 27, 2018, with Ms. D. Bordelon, Branch Chief, Technological Hazards Branch, FEMA Region VI.

On July 11, 2018, the inspectors presented the emergency preparedness exercise inspection results to W. Maguire, Site Vice President, and other members of the licensee staff.

On September 14, 2018, the inspectors presented the evaluations of changes, tests and experiments inspection results to Mr. J. Reynolds, Director, Regulatory and Performance Improvement and other members of the licensee staff.

On September 26, 2018, the inspectors presented the licensed operator requalification inspection results to Steve Vercelli, General Manager, Plant Operations.

On October 18, 2018, the inspectors presented the quarterly resident inspector inspection results to Mr. W. Maguire, Site Vice President, and other members of the licensee staff.

The inspectors confirmed that proprietary information was controlled to protect from public disclosure.

DOCUMENTS REVIEWED

71111.01Adverse Weather Protection

Calculations/Specifications

Number

Title

Revision/Date

8.3.1.32

Design Basis Flood - River Bend Station (West

Creek and Grants Bayou)

8.3.1.34

PMP in Site Area (Assuming no Berm Around

Excavation)

8.3.1.37

Determination of Water Surface Elevations in

Grants Bayou and West Creek Near Plant Site for

PMF and 25-Year Flood + SSE

CF8503290006

Peelle Design Calculation for Pressuretight and

Watertight Doors

March 15, 1985

CI8412200004

Calculations Design & Stress Analysis for

Watertight & Pressuretight Doors

December 17, 1984

RBS-210.460

Specification for Missile Protected Doors

RBS-210.461

Specification for Pressuretight Doors, Watertight

Doors, and Special Doors

RBS-210.462

Specification for Pressuretight and Watertight Doors 1

71111.04Equipment Alignment

Condition Reports (CR-RBS-)

2012-00092

2017-05633

2018-00108

2018-00402

2018-01330

2018-02069

2018-02927

2018-02956

2018-03099

2018-03687

Procedures

Number

Title

Revision

EN-LI-102

Corrective Action Program

SOP-0028

Standby Liquid Control

SOP-0031

Residual Heat Removal System

338

SOP-0035

Reactor Core Isolation Cooling System

055

71111.05Fire Protection

Calculation

Number

Title

Revision

G13.18.12.2-022

River Bend Station Combustible Loading

005

Procedures

Number

Title

Revision

AB-070-502

RHR Pump A Room Fire Area AB-5

AB-070-503

RCIC Pump Room Fire Area AB-4/Z-1 and Z-2

AB-070-504

RHR Pump C Room Fire Area AB-4/Z-1 and Z-2

RB-141-008

SLC Area Fire Area RC-4/Z-4

71111.06Flood Protection Measures

Calculations

Number

Title

Revision

PN-314

Moderate Energy Line Crack Flow Rates

PN-317

Max Flood Elevations for Moderate Energy Line

Cracks in Cat I Structures

71111.07Heat Sink Performance

Calculations

Number

Title

Revision

G13.18.2.0*031

Minimum RHR Heat Exchanger Performance

Evaluation

000

G13.18.14.0*164

Permissible Tube Blockage of RHR Heat Exchanger 000

Condition Reports (CR-RBS-)

2017-03099

2017-03109

2018-00106

2018-01330

2018-02927

Procedures

Number

Title

Revision

EN-DC-316

Heat Exchanger Performance and Condition

Monitoring

010

Procedures

Number

Title

Revision

SEP-HX-RBS-002

Performance Monitoring Program for the Residual

Heat Removal Heat Exchangers E12-EB001B and

E12-EB001D

006

71111.11Licensed Operator Requalification Program and Licensed Operator Performance

Condition Reports (CR-RBS-)

2016-00111

2016-02615

2016-06433

2017-02896

2017-04305

2018-00928

2018-02336

2018-02337

Miscellaneous

Number

Title

Date

N/A

Individual Remediation Training/Evaluation

May 25, 2017

N/A

Crew Remediation Training/Evaluation

June 29, 2017

N/A

Individual Remediation Training/Evaluation

May 18, 2018

N/A

Individual Remediation Training/Evaluation

June 6, 2018

N/A

Individual Remediation Training/Evaluation

September 14, 2017

N/A

Individual Remediation Training/Evaluation

March 30, 2018

N/A

Individual Remediation Training/Evaluation

April 18, 2018

N/A

Individual Remediation Training/Evaluation

June 6, 2018

N/A

Individual Remediation Training/Evaluation

March 2, 2018

N/A

Individual Remediation Training/Evaluation

March 14, 2018

N/A

Individual Remediation Training/Evaluation

May 9, 2017

OLTS Report 9

Active Operators Count - RBS

August 28, 2018

OLTS Report 14

License Restrictions Report - RBS

August 28, 2018

N/A

2017 Annual Operating Tests

N/A

N/A

2016 Annual Operating Tests

N/A

N/A

2018 Biennial Written Examinations

N/A

Procedures

Number

Title

Revision

1063.008

Operations Training Sequence

EN-NS-102

Fitness for Duty Program

Procedures

Number

Title

Revision

EN-NS-112

Medical Program

EN-OP-115

Conduct of Operations

25

EN-TQ-112

Medical Program

EN-TQ-114

Licensed Operator Requalification Training Program

Description

EN-TQ-200

Training Oversight Program

EN-TQ-202

Simulator Configuration Control

EN-TQ-210

Conduct of Simulator Training and Evaluations

EN-TQ-210

Conduct of Simulator Training

EN-TQ-217

Examination Security

EOP-0001

Emergency Operating Procedure - RPV

28

EOP-0002

Emergency Operating Procedure - Primary

Containment

017

EOP-0003

Emergency Operating Procedure - Secondary

Containment and Radioactive Release Control

018

TQF-201-IM05

Remedial Training Plan

71111.12Maintenance Effectiveness

Condition Reports (CR-RBS-)

2017-01980

2017-02107

2017-02470

2017-03761

2017-03976

2017-05002

2017-05033

2017-05214

2018-00398

2018-00402

2018-01022

2018-02927

2018-03099

2018-03109

Procedures

Number

Title

Revision

EN-DC-119

Equipment Database (EDB) Process and Controls

EN-DC-203

Maintenance Rule Program

EN-DC-204

Maintenance Rule Scope and Basis

EN-DC-205

Maintenance Rule Monitoring

EN-DC-206

Maintenance Rule (A)(1) Process

EN-WM-105

Planning

Procedures

Number

Title

Revision

SOP-0031

Residual Heat Removal System (Sys #204)

338

Work Order 00473239

71111.13Maintenance Risk Assessments and Emergent Work Control

Condition Reports (CR-RBS-)

2018-03715

2018-04124

Procedures

Number

Title

Revision

ADM-0096

Risk Management Program Implementation and

On-Line Maintenance Risk Assessment

27

EN-WM-104

On Line Risk Assessment

016

71111.15Operability Determinations and Functionality Assessments

Condition Reports (CR-RBS-)

2018-02828

2018-04024

2018-04458

Procedures

Number

Title

Revision

EN-OP-104

Operability Determination Process

SOP-0059

Containment HVAC System

STP-109-6802

MSIV Cold Shutdown Full Stroke Operability Test

71111.17TEvaluations of Changes, Tests and Experiments

Calculations

Number

Title

Revision

G13.18.10.1-020

Evaluation of Reactor Water Cleanup Regenerative

Heat Exchangers for the Addition of Permanent

Shielding

Calculations

Number

Title

Revision

G13.18.10.1-021

Evaluation of Reactor Water Cleanup Non-

Regenerative Heat Exchangers for the Addition of

Permanent Shielding

IA-SWP*9

Setpoint Calculation for Bistables Standby Service

Water ESX164, ESY164, ESX167, and ESY167

Standby Cooling Tower Hi-Low Level Alarm &

Minimum Water

004

PM-194

Standby Cooling Tower Performance and

Evaporation Losses Without Drywell Unit Coolers

Condition Reports (CR-RBS-)

2013-00457

2014-03977

2014-06284

2015-02190

2015-03951

2015-08410

2016-02888

2016-04095

2016-04391

2016-05997

2016-06165

2016-06393

2017-00836

2017-01253

2017-01807

2017-02330

2017-03505

2017-05572

2017-06417

2017-06428

2017-06466

2017-07080

2017-07497

2018-00613

2018-00633

2018-02207

2018-03515

2018-03621

Miscellaneous

Number

Title

Revision/Date

LAR 2016-01

Nineteenth Fuel Cycle Core Operating Limits

Report

River Bend Station Core Operating Limits Report

Cycle 19

River Bend Station Core Operating Limits Report

Cycle 19

LAR 2018-05

Twentieth Fuel Cycle Core Operating Limits Report

(COLR)

River Bend Station Core Operating Limits Report

Cycle 20

River Bend Station Core Operating Limits Report

Cycle 20

Task Qualification Matrix - F-ADM-5059 Evaluator

50.59 Evaluator Qualification

August 2, 2018

Miscellaneous

Number

Title

Revision/Date

Task Qualification Matrix - F-ADM-Screener PAD

Screener

August 2, 2018

Task Qualification Matrix - F-ADM-5059 Evaluator

50.59 Evaluator Qualification

August 9, 2018

Task Qualification Matrix - F-ADM-Screener PAD

Screener

August 9, 2018

RLO-2017-00072

Self-Assessment for Upcoming 50.59 Changes,

Test, Experiments Inspection

July 10, 2018

RBG-47776

RBF1-17-0089

Revision 25 to the Updated Safety Analysis Report

River Bend Station - Unit 1, Docket No. 50-458, 72-

049, License No. NPF-47

July 28, 2017

Procedures

Number

Title

Revision

EN-LI-100

Process Applicability Determination

EN-LI-101

CFR 50.59 Evaluations

71111.19Post-Maintenance Testing

Condition Reports (CR-RBS-)

2017-03761

2018-01022

2018-03712

2018-03715

2018-03739

2018-03748

2018-03758

2018-03772

2018-03789

2018-04419

Procedures

Number

Title

Revision

EN-WM-105

Planning

MCP-4195

Calibration of the RCIC Turbine Speed Controls

STP-309-0202

Division II Diesel Generator Operability Test

331

Work Orders

00388750

00473240

00474866

00489058

00499410

00505226

2729764

71111.22Surveillance Testing

Procedures

Number

Title

Revision

STP-000-6617

Check Valves Tested per ASME XI Inservice Testing

by Disassembly

STP-204-6303

Div I RHR Quarterly Valve Operability Test

STP-207-4537

RCIC Isolation - RCIC Steam Line Flow High

Channel Functional Test

2

Work Orders

2817537

2817540

2824009

2824164

2825270

71114.01Exercise Evaluation

Condition Reports (CR-RBS-)

2018-03659

2018-03665

2018-03669

2018-03670

2018-03791

2018-03793

Miscellaneous

Number

Title

Date

EP-M-16-020

Evaluation Report for the Exercise conducted

October 25, 2016

November 23, 2016

EP-M-17-020

Evaluation Report for the Exercise conducted

November 14, 2017

November 14, 2017

EP-M-18-005

Evaluation Report for the Exercise conducted

March 13, 2018

April 12, 2018

EP-M-18-010

Evaluation Report for the Exercise conducted

April 24, 2018

May 24, 2018

Procedures

Number

Title

Revision

River Bend Station Emergency Plan

EIP-2-001

Classification of Emergencies

26, 27

EIP-2-002

Classification Actions

EIP-2-006

Notifications

43, 44

EIP-2-007

Protective Action Recommendation Guidelines

Procedures

Number

Title

Revision

EIP-2-016

Operations Support Center

29, 30

EIP-2-018

Technical Support Center

36, 37, 38

EIP-2-020

Emergency Operations Facility

38, 39

EN-EP-610

Technical Support Center Operations

EN-EP-611

Operations Support Center Operations

Work Orders

2018-142-47

2018-142-48

2018-142-50

2018-142-51

2018-142-53

2018-142-54

2018-142-58

2018-142-60

2018-142-63

2018-142-66

2018-142-85

71114.04Emergency Plan and Emergency Action Level Changes

No additional documents were reviewed.

71114.06Drill Evaluation

Condition Reports (CR-RBS-)

2018-03659

2018-03660

2018-03666

2018-03683

2018-03791

2018-03870

2018-05221

71114.08Exercise Evaluation, Scenario Review

No additional documents were reviewed.

71151Performance Indicator Verification

Condition Reports (CR-RBS-)

2017-06728

2018-03659

2018-03666

2018-03683

Procedures

Number

Title

Revision

EN-LI-114

Regulatory Performance Indicator Process

& 12

EPP-2-701

Prompt Notification System Maintenance and

Testing

NEI 99-02

Regulatory Assessment Performance Indicator

Guideline

Work Orders

2757383 01

2809147 01

71153Follow-up of Events and Notices of Enforcement Discretion

Condition Reports(CR-RBS-)

2017-02790

2018-02687

2018-02768

2018-02775

2702Follow-up on Traditional Enforcement Actions Including Violations, Deviations,

Confirmatory Action Letters, Confirmatory Orders, and Alternative Dispute Resolution

Confirmatory Orders

Miscellaneous

Number

Title

Date

RBG-47771

RBF1-17-0080

Reply to Notice of Violation 05000458/2017-009-01;

River Bend Station - Unit 1

Docket No. 50-458

License No. NPF-47

July 6, 2017

RBG-47823

Request for Review and Approval of Relocation of

the Reactor Core Isolation Cooling (RCIC) Injection

Point from the Reactor Vessel Head Spray Nozzle

to the A Feedwater Line via the A Residual Heat

Removal (RHR) Shutdown Cooling Return Line

River Bend Station - Unit 1

Docket No. 50-458

License No. NPF-47

January 29, 2018

ML18313A028

SUNSI Review:

ADAMS:

Non-Publicly Available

Non-Sensitive

Keyword:

By: DLP

Yes No

Publicly Available

Sensitive

NRC-003

OFFICE

ASRI:DRP/C

RI:DRP/C

SPE:DRP/C

C:DRS/EB1

C:DRS/EB2

C:DRS/OB

NAME

CSpeer

BParks

DProulx

TFarnholtz

GWerner

VGaddy

SIGNATURE

CAS

BP

DLP

TRF

GEW

Vgg

DATE

10/31/18

10/31/18

10/29/18

10/29/2018

10/29/2018

10/30/18

OFFICE

C:DRS/PSB2

TL:IPAT

BC:DRP/C

NAME

HGepford

GMiller

JKozal

SIGNATURE

hjg

gbm

DLP

DATE

10/29/18

10/31/18

11/8/18