IR 05000277/2018003

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Integrated Inspection Report 05000277/2018003 and 05000278/218003, Preliminary White Finding, and Exercise of Enforcement Discretion
ML18317A003
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 11/13/2018
From: David Pelton
Division Reactor Projects I
To: Bryan Hanson
Exelon Generation Co, Exelon Nuclear
Greives J
References
EA-18-107, EA-18-108 IR 2018003
Download: ML18317A003 (36)


Text

UNITED STATES ber 13, 2018

SUBJECT:

PEACH BOTTOM ATOMIC POWER STATION - INTEGRATED INSPECTION REPORT 05000277/2018003 AND 05000278/2018003, PRELIMINARY WHITE FINDING, AND EXERCISE OF ENFORCEMENT DISCRETION

Dear Mr. Hanson:

On September 30, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Peach Bottom Atomic Power Station (Peach Bottom), Units 2 and 3. On October 23, 2018, the NRC inspectors discussed the results of this inspection with Mr. Pat Navin, Peach Bottom Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

The enclosed inspection report discusses a finding that the NRC has preliminarily determined to be White, a finding with low to moderate increased safety significance that may require additional NRC inspections. As described in the enclosed report, the finding is associated with an apparent violation of Title 10 of the Code of Federal Regulations (CFR) Part 50, Appendix B, Criterion XVI, Corrective Action, because Exelon did not establish measures to assure that conditions adverse to quality associated with the E-3 emergency diesel generator (EDG)

scavenging air check valve were promptly identified and corrected which resulted in a failure of the E-3 EDG on June 13, 2018. As a consequence, Exelon also violated Peach Bottom Units 2 and 3 Technical Specification (TS) 3.8.1, since the E-3 EDG was determined to be inoperable for greater than the TS allowed outage time. The finding was assessed based on the best available information using Inspection Manual Chapter (IMC) 0609.04, Initial Characterization of Findings, issued October, 7, 2016, and Exhibit 2 of IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, issued June 19, 2012. The basis for the NRCs preliminary significance determination is described in the enclosed report.

As an apparent violation of NRC requirements, this finding is being considered for escalated enforcement action in accordance with the Enforcement Policy, which can be found on the NRCs Website at https://www.nrc.gov/about-nrc/regulatory/enforcement/enforce-pol.html. In accordance with IMC 0609, we intend to complete our evaluation and issue our final safety significance determination within 90 days from the date of this letter. The NRCs SDP is designed to encourage an open dialogue between your staff and the NRC; however, the dialogue should not affect the timeliness of our final determination. We believe that we have sufficient information to make a final significance determination.

However, before we make a final decision, we are providing you an opportunity to provide your perspective on this matter, including the significance, causes, and corrective actions, as well as any other information that you believe the NRC should take into consideration. Accordingly, you may notify us of your decision within 10 days from the issue date of this letter to: (1) request a regulatory conference to meet with the NRC and provide your views in person, (2) submit your position on the finding in writing, or (3) accept the finding as characterized in the enclosed inspection report.

If you choose to request a regulatory conference, the meeting should be held in the NRC Region I office within 40 days of your receipt of this letter, and will be open for public observation. The NRC will issue a public meeting notice and a press release to announce the date and time of the conference. We encourage you to submit supporting documentation at least one week prior to the conference in an effort to make the conference more efficient and effective. If you choose to provide a written response, it should be sent to the NRC within 40 days of your receipt of this letter. You should clearly mark the response as Response to Preliminary White Finding and Apparent Violation in Inspection Report No. 05000277/2018003 and 05000278/2018003; EA-18-107, and send it to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to the Regional Administrator, Region I, and the NRCs Resident Inspector at Peach Bottom.

You may also elect to accept the finding as characterized in this letter and the inspection report, in which case the NRC will proceed with its regulatory decision. However, if you decline to request a regulatory conference or to submit a written response, you relinquish your right to appeal the NRCs final significance determination, in that by not doing either, you would fail to meet the appeal requirements stated in the Prerequisite and Limitation sections of Attachment 2 of IMC 0609.

Please contact Jonathan Greives at 610-337-5337 within 10 days from the issue date of this letter to notify the NRC of your intentions. If we have not heard from you within 10 days, we will continue with our significance determination and enforcement decision.

Because the NRC has not made a final determination in this matter, no Notice of Violation is being issued for this inspection finding at this time. In addition, please be advised that the number and characterization of the apparent violation may change based on further NRC review. The final resolution of this matter will be conveyed in separate correspondence.

In addition, the NRC reviewed Licensee Event Report 05000278/2018-001-00, which described the circumstances associated with a failed reactor core isolation cooling (RCIC) turbine exhaust pressure switch. It was recognized that this failed switch resulted in the Unit 3 RCIC system being inoperable for a period of time that exceeded the allowed outage time of fourteen days detailed in TS 3.5.3, and therefore, was a violation of TSs. A Region I Senior Reactor Analyst (SRA) performed a risk evaluation and determined the issue was of low to moderate safety significance (White).

Although this issue constituted a violation of NRC requirements, the NRC determined that the pressure switch failure which caused the Unit 3 RCIC system to be inoperable was not within Exelons ability to reasonably foresee and correct. As a result, the NRC did not identify a performance deficiency associated with this condition. The NRCs assessment considered Exelons maintenance practices, industry operating experience, vendor and industry maintenance, and testing recommendations. Based on the results of the NRCs inspection and assessment of the RCIC issue, I have been authorized, after consultation with the Director, Office of Enforcement, to exercise enforcement discretion in accordance with NRC Enforcement Policy Section 2.2.4, Exceptions to Using Only the Operating Reactor Assessment Program, and Section 3.10, Reactor Violations with No Performance Deficiency. The Region I Regional Administrator was also consulted regarding enforcement discretion for this issue.

Finally, NRC inspectors documented one finding of very low safety significance (Green) in this report. The finding involved a violation of NRC requirements. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violation or significance of the NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRCs Resident Inspector at Peach Bottom. In addition, if you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U. S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I, and the NRCs Resident Inspector at Peach Bottom.

In accordance with 10 CFR Part 2.390, Public Inspections, Exemptions, Requests for Withholding, this letter, its enclosure, and your response (if any) will be made available for public inspection and copying in the NRCs Agencywide Documents Access and Management System (ADAMS), accessible from the NRCs Website at http://www.nrc.gov/reading-rm/adams.html and in the NRCs Public Document Room.

Sincerely,

/RA/

David L. Pelton, Acting Director Division of Reactor Projects Docket Numbers: 50-277 and 50-278 License Numbers: DPR-44 and DPR-56

Enclosure:

Inspection Report 05000277/2018003 and 05000278/2018003 w/Attachment:

E-3 Emergency Diesel Generator Failure Detailed Risk Evaluation

Inspection Report

Docket Numbers: 50-277 and 50-278 License Numbers: DPR-44 and DPR-56 Report Numbers: 05000277/2018003 and 05000278/2018003 Enterprise Identifier: I-2018-003-0070 Licensee: Exelon Generation Company, LLC Facility: Peach Bottom Atomic Power Station, Units 2 and 3 Location: Delta, Pennsylvania Inspection Dates: July 1, 2018 to September 30, 2018 Inspectors: J. Heinly, Senior Resident Inspector B. Smith, Resident Inspector J. Bridge, Acting Resident Inspector F. Arner, Senior Reactor Inspector D. Beacon, Project Engineer C. Bickett, Senior Reactor Inspector J. Cassata, Health Physics Inspector M. Orr, Reactor Inspector J. Schoppy, Reactor Engineer Approved By: David L. Pelton, Acting Director Division of Reactor Projects Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Exelons performance at

Peach Bottom Atomic Power Station (Peach Bottom), Units 2 and 3, by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC-identified and self-revealed findings, violations, and additional items are summarized in the table below.

List of Findings and Violations High Pressure Coolant Injection System Exhaust Pressure Switches Exceeded Documented Qualified Life Cornerstone Significance Cross-cutting Report Aspect Section Mitigating Green P.2 - Problem 71152 Systems NCV 05000277/2018003-01 Identification and Closed Resolution,

Evaluation The inspectors identified a Green non-cited violation (NCV) of Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Appendix B, Criterion III, Design Control, because Exelon did not establish measures to ensure that environmental qualification requirements for qualified components were correctly translated into procedures and instructions. Specifically, the end-of-life replacement requirements for the Unit 2 high pressure coolant injection (HPCI) exhaust pressure switches were not translated into maintenance procedures and instructions. As such,

Exelon did not replace the switches prior to the end of their documented qualified life.

Inadequate Corrective Actions Result in the Failure of the E-3 Emergency Diesel Generator Cornerstone Significance Cross-Cutting Report Aspect Section Mitigating Preliminary White H.11 - Human 71153 Systems AV 05000277/2018003-02 Performance,

EA-18-107 Challenge the Opened Unknown The inspectors identified a self-revealing preliminary White finding associated with an apparent violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, because Exelon did not perform adequate corrective actions on the E-3 emergency diesel generator (EDG)scavenging air check valve assembly. Specifically, Exelon did not perform an adequate repair of an interference fit pin joint during maintenance activities in April 2017 and did not correct an oil leak on the check valve dashpot assembly identified in September 2017, which resulted in the E-3 EDG failure on June 13, 2018.

Additional Tracking Items Type Issue number Title Inspection Status Results Section LER 05000277/2018-002-00 EDG Air Inlet Check 71153 Closed Valve Failure Results in a Condition Prohibited by Technical Specification (TS)

LER 05000278/2018-001-00 Reactor Core Isolation 71153 Closed Cooling (RCIC) System Pressure Switch Failure Results in Condition Prohibited by TS

TABLE OF CONTENTS

PLANT STATUS

INSPECTION SCOPES

................................................................................................................

REACTOR SAFETY

................................................................................................................

RADIATION SAFETY

..............................................................................................................

OTHER ACTIVITIES - BASELINE

.........................................................................................

INSPECTION RESULTS

..............................................................................................................

EXIT MEETINGS AND DEBRIEFS

............................................................................................ 17

DOCUMENTS REVIEWED

......................................................................................................... 18

ATTACHMENT: E-3 EMERGENCY DIESEL GENERATOR FAILURE DETAILED RISK

EVALUATION ............................................................................................................... A-1

PLANT STATUS

Unit 2

The unit remained at or near rated thermal power (RTP) for the inspection period.

Unit 3

Unit 3 began the inspection period at RT

P. On September 7, 2018, the unit was down powered

to 29 percent thermal power to perform scheduled maintenance and returned to RTP on

September 9, 2018. On September 22, 2018, the unit was shutdown to repair a pressure

boundary leak from am instrument line associated with the HPCI system. The unit was returned

to RTP on September 25, 2018. On September 30, 2018, the unit experienced an automatic

reactor scram from RTP when two of three main condensate pumps tripped due to a failed

electrical power cable, and remained shutdown through the end of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed plant status activities described in

IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152,

Problem Identification, and Resolution. The inspectors reviewed selected procedures and

records, observed activities, and interviewed personnel to assess Exelons performance and

compliance with Commission rules and regulations, license conditions, site procedures, and

standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

External Flood (1 Sample)

The inspectors evaluated diesel generator building inoperable flood seals on

August 16, 2018.

71111.04 - Equipment Alignment

Partial Walkdowns (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1) Unit 2 A core spray (CS) with B CS out of service on July 10, 2018

(2) Unit 2 and Unit 3 E-1, E-2, E-3 with E-4 EDGs inoperable on September 17, 2018

(3) Unit 3 high pressure service water (HPSW) following pump, valve, and flow test on

September 28, 2018

71111.05A/Q - Fire Protection Annual/Quarterly

Quarterly Inspection (4 Samples)

The inspectors evaluated fire protection program implementation in the following selected

areas:

(1) Unit 2 and Unit 3 cable spreading room on July 30, 2018

(2) Unit 3 B/D residual heat removal rooms on August 22, 2018

(3) Unit 2 A battery room on August 23, 2018

(4) Unit 2 B 4kilovolt (kV) switchgear room on August 23, 2018

Annual Inspection (1 Sample)

The inspectors evaluated fire brigade performance to an actual fire in the Unit 3 HPSW

room on July 23, 2018. The fire was small, isolated, did not affect any safety-related

equipment, and was promptly extinguished such that no emergency action level declarations

was required.

71111.06 - Flood Protection Measures

Internal Flooding (1 Sample)

The inspectors evaluated internal flooding mitigation protections in the Unit 2 and Unit 3

standby gas room and radwaste basement (91) from July 23, 2018, through July 27, 2018.

71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance

Operator Requalification (1 Sample)

The inspectors observed and evaluated licensed operator requalification training on

August 6, 2018.

Operator Performance (1 Sample)

The inspectors observed and evaluated a Unit 3 summer load drop on September 8, 2018,

and a rod pattern adjustment on September 11, 2018.

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness (3 Samples)

The inspectors evaluated the effectiveness of routine maintenance activities associated with

the following equipment and/or safety significant functions:

(1) Unit 2 and Unit 3 reactor recirculation pump motor adjustable speed drives on July 23,

2018, through July 27, 2018

(2) Unit 3 RCIC on August 22, 2018

(3) Unit 2 and Unit 3 EDGs on September 6, 2018

71111.13 - Maintenance Risk Assessments and Emergent Work Control (5 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent work

activities:

(1) Unit 3 RCIC pressure switch calibration on September 10, 2018

(2) Unit 2 automatic depressurization system (ADS) logic system functional test on

September 12, 2018

(3) Unit 2 and Unit 3 E-4 EDG 24-hour endurance run with offsite line 343 out of service on

September 17, 2018

(4) Unit 3 HPCI logic system functional test on September 19, 2018

(5) Unit 2 and Unit 3 E-2 EDG instrumentation logic test on September 20, 2018

71111.15 - Operability Determinations and Functionality Assessments (3 Samples)

The inspectors evaluated the following operability determinations and functionality

assessments:

(1) Unit 2 and Unit 3 EDGs external flood seal deficiencies on August 23, 2018

(2) Unit 2 and Unit 3 containment atmosphere control / containment atmosphere dilution

primary containment isolation valve failure on September 14, 2018

(3) Unit 3 HPCI differential pressure indicating switch failure on September 21, 2018

71111.19 - Post-Maintenance Testing (4 Samples)

The inspectors evaluated post-maintenance testing for the following maintenance/repair

activities:

(1) Unit 3 A HPSW ventilation repair on August 15, 2018

(2) Unit 3 ADS valve replacement on September 11, 2018

(3) Unit 3 HPCI sensing line leak repair on September 24, 2018

(4) Unit 2 and Unit 3 diesel driven fire pump 2-year overhaul on September 27, 2018

71111.20 - Refueling and Other Outage Activities (1 Sample)

The inspectors evaluated the Unit 3 forced outage activities from September 22, 2018, to

September 26, 2018.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Routine (4 Samples)

(1) E-4 EDG slow start on July 25, 2018

(2) E-2 EDG alternative shutdown control functional on August 10, 2018

(3) Unit 3 nitrogen backup to ADS on August 22, 2018

(4) Unit 3 RCIC pressure switch calibration on September 10, 2018

RADIATION SAFETY

71124.07 Radiological Environmental Monitoring Program

Site Inspection (1 Sample)

The inspectors verified that the Radiological Environmental Monitoring Program quantified

the impact of radioactive effluent releases to the environment and sufficiently validated the

integrity of the radioactive gaseous and liquid effluent release program.

The inspectors verified that the Radiological Environmental Monitoring Program was

consistently implemented with the licensees TSs and/or Offsite Dose Calculation Manual

and validated that the program meets the design objectives in Appendix I to 10 CFR Part 50.

Groundwater Protection Initiative Implementation (1 Sample)

The inspectors verified that the licensee is continuing to implement the voluntary Nuclear

Energy Institute/Industry Ground Water Protection Initiative.

OTHER ACTIVITIES - BASELINE

71152 - Problem Identification and Resolution

Annual Follow-up of Selected Issues (2 Samples)

The inspectors reviewed Exelons implementation of its corrective action program (CAP)

related to the following issues:

(1) Issue Report (IR) 4050431, Water Found in HPCI Lube Oil System

(2) IR 4146368, HPCI System Exhaust Pressure Switch Environmental Qualification Life

Evaluation

71153 - Follow-up of Events and Notices of Enforcement Discretion

Events (1 Partial Sample)

The inspectors evaluated operator response to the following event.

(1) Unit 3 SCRAM on September 30, 2018. The initial evaluation of this event was in

progress as of the close of this inspection period. The final evaluation of this event will

be conducted during a future inspection.

Licensee Event Reports (LERs) (2 Samples)

The inspectors evaluated the following Exelon event reports which can be accessed at

https://lersearch.inl.gov/LERSearchCriteria.aspx:

(1) LER 05000277/2018-002-00, E-3 EDG Air Inlet Check Valve Failure Results in a

Condition Prohibited by TS (ADAMS Accession No. ML18222A326)

(2) LER 05000278/2018-001-00, RCIC System Pressure Switch Failure Results in Condition

Prohibited by TS (ADAMS Accession No. ML18172A260)

INSPECTION RESULTS

HPCI System Exhaust Pressure Switches Exceeded Documented Qualified Life

Cornerstone Significance Cross-cutting Report

Aspect Section

Mitigating Green P.2 - Problem 71152

Systems NCV 05000277/2018003-01 Identification

Closed and Resolution,

Evaluation

The inspectors identified a Green NCV of 10 CFR Part 50, Appendix B, Criterion III, Design

Control, because Exelon did not establish measures to ensure that environmental

qualification requirements for qualified components were correctly translated into procedures

and instructions. Specifically, the end-of-life replacement requirements for the Unit 2 HPCI

exhaust pressure switches were not translated into maintenance procedures and instructions.

As such, Exelon did not replace the switches prior to the end of their documented qualified

life.

Description: In response to NRC inspectors questions related to failure of the RCIC system

exhaust pressure switch, the station reviewed the environmental qualification binder for the

Unit 2 HPCI system exhaust pressure switches, which are of similar construction, and located

in a similar service environment. Environmental Qualification Binder EQ-PB-026, Static O-

Ring Pressure Switch, stated that the HPCI system exhaust pressure switches were to be

replaced every 43 years in order to maintain their environmental qualification. To meet this

requirement, the switches should have been replaced no later than 2016.

A review of the maintenance history for the HPCI system pressure switches noted that there

were no preventive maintenance replacement tasks for these components, and the switches

had not been replaced as a result of corrective maintenance over the life of the plant. As

such, these pressure switches had exceeded their documented qualified life. The inspectors

determined that this represented a non-conforming condition and reasonable doubt existed as

to the ability of these pressure switches to perform their safety function in a harsh

environment during an event.

Exelon originally calculated the 43-year service life based on a design service temperature of

85°F, as documented in NE-00164, Specification for Environmental Service Conditions -

Peach Bottom Atomic Power Stations Units 2 and 3. In response to the current issue,

Exelon evaluated operability using actual temperature data collected quarterly since 1995 per

Peach Bottom routine test RT-I-094-800-2, Reactor Building Ambient Temperature Data

Collection, and determined a new service temperature of approximately 82°F. Using this

revised value, Exelon calculated a new qualified life of 51 years for the HPCI system pressure

switches which extended the replacement date to 2024. Based on a review of this

temperature data, the technical evaluation that documented the life extension, and a field

walkdown of the switches, the inspectors determined that Exelons conclusion was

reasonable.

The inspectors also determined that the station had a prior opportunity to identify this

condition. Following identification of a similar issue with static O-ring pressure switches on

the residual heat removal system in April 2017, as documented in IR 3997737, Exelon

conducted an extent of condition review. However, this extent of condition review failed to

identify this issue with the HPCI system exhaust pressure switches, even though the switches

are from the same manufacturer, and are documented in the same environmental

qualification binder (EQ-PB-026).

Corrective Actions: Exelon entered this issue into the CAP as IR 4146368, and calculated a

new qualified life of 51 years based on actual service temperatures in the room. As of the

date of this inspection, replacement of the HPCI system exhaust pressure switches was

planned as corrective maintenance for early 2019.

Corrective Action Reference: IR 4146368

Performance Assessment:

Performance Deficiency: The failure to establish measures to ensure that environmental

qualification requirements for qualified components were correctly translated into procedures

and instructions in accordance with 10 CFR Part 50, Appendix B, Criterion III, Design

Control, was a performance deficiency.

Screening: The performance deficiency was more than minor because this issue adversely

impacted the equipment performance attribute of the Mitigating Systems cornerstone

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. This issue is also similar to more-

than-minor examples 3.j and 3.k presented in IMC 0612, Appendix E, Examples of Minor

Issues. Specifically, this performance deficiency resulted in a condition where there was

reasonable doubt as to the operability and reliability of the Unit 2 HPCI exhaust pressure

switches. As such, Peach Bottom needed to conduct an additional engineering evaluation to

extend the service life of the exhaust pressure switches, thus justifying that the switches

would continue to perform their safety function.

Significance: The inspectors assessed the significance of the finding using Exhibit 2 of IMC

0609, Appendix A, The SDP for Findings At-Power. The inspectors determined the finding

was of very low safety significance (Green) because the finding was a deficiency affecting the

reliability of a mitigating structure, system, or component, and the structure, system, or

component maintained its operability or functionality. Specifically, the safety function of the

HPCI system was not lost based upon a technical evaluation which extended the

environmental qualification life of the Unit 2 HPCI system exhaust pressure switches from 43

to 51 years.

Cross-cutting Aspect: This finding had a cross-cutting aspect in the area of Problem

Identification and Resolution, Evaluation, because Exelon did not conduct a thorough extent

of condition evaluation following identification of a similar issue with residual heat removal

pump discharge pressure switches in 2017. Specifically, the stations extent of condition

review failed to identify a similar issue with the Unit 2 HPCI system exhaust pressure

switches, even though the switches are from the same manufacturer, and are documented in

the same environmental qualification binder [P.2].

Enforcement:

Violation: 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part, that

measures shall be established to assure that applicable regulatory requirements and the

design basis are correctly translated into specifications, drawings, procedures, and

instructions.

Contrary to the above, prior to June 12, 2018, Exelon failed to ensure that the design basis

was translated into procedures and instructions. Specifically, Exelon did not incorporate the

environmental qualification requirement associated with end-of-life replacement of the Unit 2

HPCI exhaust pressure switches into preventive maintenance procedures.

Disposition: This violation is being treated as a NCV, consistent with Section 2.3.2 of the

Enforcement Policy.

Observations 71152

On September 9, 2017, Exelon staff initiated corrective action IR 4050431 for water found in

the Unit 3 HPCI turbine lube oil reservoir during a weekly HPCI auxiliary oil pump operability

test (RT-O-023-302-3). Operators were taking weekly HPCI lube oil samples in accordance

with an existing adverse condition monitoring plan (ACMP) initiated in May 2017 in response

to a rise in HPCI thrust bearing and casing temperatures (IR 4004135). Operators drained the

water from the lube oil reservoir. Operators, with engineering support, promptly evaluated

HPCI system operability (including past operability) and determined that HPCI remained

operable. Exelon staff revised the existing HPCI lube oil monitoring ACMP to also include

daily lube oil reservoir samples to ensure water content remained below threshold limits and

to drain any water found.

Exelon staff implemented the ACMP to monitor HPCI turbine temperatures and lube oil

moisture content in response to identified leakage past the Unit 3 HPCI steam supply valve

(MO-3-23-014) that resulted in steam condensation in the turbine casing and on the casing

insulation and subsequent water intrusion into the lube oil system. The larger quantity of

water found in the lube oil reservoir on September 9, 2017, was unexpected and not

consistent with the previous ACMP sampling results and trending (including the sample taken

on September 2, 2017). Engineering determined that the most likely cause of the additional

water found in the reservoir was from stroking the HPCI steam supply valve (MO-3-23-014) on

August 31, 2017, during a post-maintenance test following a relay contact replacement

without fully operating the HPCI system. Stroking the steam supply valve with the

downstream HPCI stop and control valves closed allowed steam to condense between the

HPCI supply and stop valves. Subsequently, when the stop and control valves were stroked

during the weekly HPCI auxiliary oil pump operability test, the condensed steam had a path to

the turbine casing and lube oil system.

During the Unit 3 refueling outage (3R21) in October 2017, Exelon staff resolved the MO-3-

23-014 leak-by issue under work orders to open and inspect the valve, perform in-body

repairs, perform preventive maintenance, and upgrade the actuator (Work Orders 04306865,

04306866, and 04181415). In addition, Exelon staff initiated a corrective action to provide

additional guidance and/or precautions while cold stroking the HPCI steam supply valve at

power (4050431-11).

Based on a review of Unit 3 HPCI operating parameters, system walkdowns, and lube oil

sample results, the inspectors noted that Exelons refueling outage work activities on the

steam supply valve effectively addressed the leak-by issue. The inspectors also reviewed

Exelons corrective actions associated with a similar active Unit 2 ACMP addressing

increased monitoring for identified leakage past the Unit 2 HPCI steam supply valve

(MO-2-23-014). The inspectors concluded that Exelon staff had taken timely and appropriate

actions in accordance with Exelons procedures and CAP, and 10 CFR Part 50, Appendix B

and evaluated operability with sufficient technical rigor to support their conclusions. The

inspectors determined that Exelon staffs associated engineering evaluations and trending

were sufficiently thorough and based on the best available information, sound judgment, and

relevant operating experience. The assigned corrective actions were aligned with engineering

evaluations, adequately tracked, appropriately documented, and completed as scheduled.

Based on the documents reviewed, HPCI and RCIC system walkdowns, and discussions with

engineering personnel, the inspectors noted that Exelon personnel identified problems and

entered them into the CAP at a low threshold.

Inadequate Corrective Actions Result in the Failure of the E-3 EDG

Cornerstone Significance Cross-cutting Report

Aspect Section

Mitigating Preliminary White H.11 - Human 71153

Systems AV 05000277/278/2018003-02 Performance,

Opened Challenge the

Enforcement Action (EA)-18-107 Unknown

Introduction: The inspectors identified a self-revealing preliminary White finding associated

with an apparent violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action,

because Exelon did not perform adequate corrective actions on the E-3 EDG scavenging air

check valve assembly. Specifically, Exelon did not perform an adequate repair of an

interference fit pin joint during maintenance activities in April 2017 and did not correct an oil

leak on the check valve dashpot assembly identified in September 2017, which resulted in the

E-3 EDG failure on June 13, 2018.

Description: Peach Bottom has four, 12 cylinder Fairbank Morse EDGs that supply

emergency power to both Unit 2 and Unit 3. Each EDG contains a scavenging air system

which provides compressed cool combustion air into the cylinders. The scavenging air input

to the cylinders is shared between the blower (supercharger) and the two parallel turbo

chargers. The scavenging air check valve controls the contribution of air input between the

blower and outside air to the turbochargers. The check valve is connected to a shaft through

an interference fit pin and the shafts movement is limited/dampened by an oil filled dashpot.

At low loads, the air input to the turbo charger is provided by the blower (scavenging air check

valve closed) and at high loads the check valve opens to supplement the turbo charger

suction with room air.

On April 1, 2017, during a routine preventive maintenance overhaul of the E-3 EDG, station

technicians identified radial play and looseness of the scavenging air check valve on its shaft.

The condition was entered in the CAP under IR 3992819. The station determined that the

cause of the looseness was wear between the shaft, check valve, and interference fit pin. An

engineering change package was developed to remove the interference fit pin, ream out the

hole in the shaft and check valve to a larger size, and manufacture a new interference fit pin.

This first time evolution repair was completed during the planned overhaul and the EDG

successfully passed its post-maintenance testing on April 6, 2017.

On September 20, 2017, the NRC inspectors observed a full load surveillance test of the E-3

EDG and identified an oil leak on the scavenging air check valve dashpot. The station

documented the condition under IR 4054092 and determined that the E-3 EDG was operable

because the amount of oil loss during the test (1 drop per 3 minutes) was low and would not

impact the dashpot function. However, an interim corrective action was established to refill

the oil in the dashpot after each surveillance test run to ensure that adequate inventory in the

dashpot remained to support its design function.

On June 13, 2018, during a quarterly full load surveillance test, the E-3 EDG was operating at

full load when elevated exhaust temperatures were observed and a metallic noise was heard

near the turbocharger assembly. The operators emergently shut down the EDG, declared it

inoperable, and entered the condition into their CAP under IR 4146926. The turbo charger

was inspected and technicians identified that the scavenging air check valve interference fit

pin had become displaced from the shaft and entered/damaged the suction side of the

aluminum turbo charger compressor blades. The aluminum debris from the damaged blades

migrated through the scavenging air inlet and into the diesel generator cylinders and

contaminated the diesel generator lube oil and exhaust systems. Exelon performed

immediate corrective actions to include an extensive emergent overhaul of the diesel

generator to remove all of the contaminants and inspect, assess, and replace critical internal

components, as necessary. In addition, the site replaced the scavenging air check valve

assembly along with the supporting dashpot assembly. The inspectors performed extensive

inspection and assessment of Exelons corrective actions and post-maintenance testing and

did not identify any additional issues of concern. The E-3 EDG successfully passed its post-

maintenance testing on June 23, 2018. The inspectors evaluated the extent of condition and

determined that the scavenging air check valve assemblies on the other three EDGs had

been recently inspected and no conditions adverse to quality had been identified.

Furthermore, no repairs had been performed to the scavenging air check valve assemblies on

the other three EDGs.

Exelon performed a cause evaluation to determine the apparent and contributing causes that

led to the interference fit pin becoming displaced and damaging the E-3 EDG. Exelon

determined that the apparent cause was that the interference fit pin repair in April 2017 was

inadequate. Specifically, the hole through the shaft and check valve was not cleanly reamed

and the interference fit pin was undersized which resulted in insufficient interference between

the pin, shaft, and check valve body. Furthermore, it was identified that the leaking dashpot

assembly had not been refilled with oil after every diesel run, as recommended through the

CAP, and was found with low oil level. The degraded dashpot allowed greater forces to be

exerted on the check valve, shaft, and pin assembly and contributed to the pin becoming

dislodged.

Corrective Actions: Exelon performed immediate corrective actions on the E-3 EDG to

include the replacement of the scavenging air check valve and dashpot assembly, clean the

internal contaminants, and inspect, assess, and replace critical internal components as

necessary. Furthermore, Exelon plans to perform training/briefings on the inadequate

maintenance/engineering practices that contributed to the failure.

Corrective Action Reference: IR 4146926

Performance Assessment:

Performance Deficiency: The inspectors identified that the failure to perform adequate

corrective actions to address the degraded scavenging air check valve assembly which

resulted in the E-3 EDG failure was a performance deficiency that was within Exelons ability

to foresee and correct. Specifically, the E-3 EDG was declared inoperable due to the

inadequate corrective actions associated with the scavenging air check valve interference pin

repair and the leaking dashpot assembly.

Screening: The finding was more than minor, because it was associated with the equipment

performance attribute of the Mitigating Systems cornerstone and adversely impacted the

cornerstone objective to ensure the availability of systems that respond to initiating events to

prevent undesirable consequences (i.e., core damage). Specifically, the E-3 EDG was

unavailable to perform its safety function as a result of Exelons inadequate corrective

actions.

Significance: The inspectors evaluated the significance of this finding using IMC 0609,

Appendix A, The SDP for Findings at Power, Exhibit 2 - Mitigating Systems Screening

Questions. The inspectors determined that the finding resulted in the actual loss of function

of a single train (E-3 EDG) for longer than its allowed TS outage time and required a detailed

risk evaluation.

A Region I Senior Reactor Analyst (SRA) performed a detailed risk evaluation. The finding

was preliminarily determined to be of low to moderate safety significance (White). The risk

important sequences were dominated by external fire risk. Specifically, a postulated fire in

the 4kV switchgear rooms. The internal event risk was dominated by a weather related loss

of offsite power, operator failure to establish a Conowingo tie line setup, failure of the E-2

EDG to run, failure to recover an EDG, failure to cross tie emergency busses, failure to

recover offsite power, and a failure of RCI

C. See Attachment, E-3 EDG Failure Detailed Risk

Evaluation, for a detailed review of the quantitative criteria considered in the preliminary risk

determination.

Cross-Cutting Aspect: The inspectors determined this finding had a cross-cutting aspect in

the area of Human Performance, Challenge the Unknown, because Exelon did not

adequately challenge the risks involved with the first time evolution repair on the scavenging

air check valve and the degraded/leaking dashpot condition. The risks were not well

understood and inadequately managed through the CAP. [H.11]

Enforcement:

Apparent Violation:

CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires that measures shall

be established to assure conditions adverse to quality are promptly identified and corrected.

Peach Bottom Units 2 and 3 TS 3.8.1 requires all four EDGs to be operable in Mode 1 and if

any one EDG is determined to be inoperable, it shall be returned to an operable status within

days or the unit shall be shut down and in Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

Contrary to the above, from April 1, 2017, to June 13, 2018, Exelon did not establish

measures to assure that conditions adverse to quality associated with the E-3 EDG

scavenging air check valve were promptly identified and corrected. Specifically, after

identifying on April 1, 2017, that the E-3 EDG scavenging air check valve was loose due to

wear around the interference fit pin and identifying on September 20, 2017, that there was an

oil leak on the scavenging air check valve dashpot, Exelon did not take adequate corrective

actions to address the adverse conditions. As a result, on June 13, 2018, during a quarterly

surveillance test, the scavenging air check valve interference fit pin dislodged from the shaft

and entered/damaged the suction side of the aluminum turbo charger compressor blades.

Consequently, the E-3 EDG was rendered inoperable prior to June 13, 2018, for a period

longer than its TS allowed outage time, and the unit had not been shut down and placed in

Mode 3.

Disposition: This violation is being treated as an apparent violation (AV) pending a final

significance determination. The disposition of this violation closes LER 05000277/2018-002-

00.

Reactor Core Isolation Cooling System Pressure Switch Failure Results in Condition

Prohibited by TS

Enforcement EA-18-108 71153

Discretion

Description: On April 22, 2018, during a routine surveillance test of the RCIC system, the

RCIC turbine tripped approximately 28 seconds after startup, prior to the system reaching

rated flow and pressure. Concurrent with the RCIC trip, an alarm was received for RCIC

turbine high exhaust pressure; however, local indications did not indicate a true high pressure

in the exhaust line. Therefore, the RCIC system was declared inoperable and TS 3.5.3,

Condition A was entered, which requires the RCIC system to be restored to operable within

days. Troubleshooting determined that the B RCIC exhaust pressure switch (PS-3-13-

2b) had prematurely tripped at normal operating pressure due to an age-related failure of the

instrument diaphragm and O-ring. The RCIC system had been previously verified as

operable during its last surveillance run on January 16, 2018.

Corrective Actions: The failed pressure switch was replaced and the station performed an

extent of condition review/inspection of similar pressure switch instruments. Following

replacement of the switch, RCIC was retested and restored to operable on April 23, 2018.

Furthermore, actions were established to modify the turbine trip logic to remove the single

point trip vulnerability.

Corrective Action Reference: IR 4129583

Enforcement:

Violation: Peach Bottom Unit 3 TS 3.5.3 requires that the RCIC system shall be operable in

Mode 1, and if RCIC becomes inoperable, it shall be returned to operable status within 14

days or the plant shall be placed in Mode 3 within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

Contrary to the above, based on relevant causal information, Unit 3 RCIC was likely

inoperable prior to April 22, 2018, for a period greater than the TS allowed outage time of 14

days, and Unit 3 had not been placed in Mode 3. Specifically, on April 22, 2018, the Unit 3

RCIC turbine tripped during startup for a routine surveillance test due to a degraded turbine

exhaust pressure switch which resulted in an inoperability time of greater than 14 days.

Internal inspection on the switch identified that it failed due to corrosion from water intrusion

which had existed for an extended period of time.

Severity/Significance: For violations warranting enforcement discretion, IMC 0612 does not

require a detailed risk evaluation; however, safety significance characterization is appropriate.

A Region I SRA performed a best estimate analysis of the safety significance using the Peach

Bottom Unit 3 Standardized Plant Analysis Risk (SPAR) model, Version 8.51 and Systems

Analysis Programs for Hands-On Integrated Reliability Evaluations (SAPHIRE), Version 8.1.8.

This model was used to evaluate the internal events increase in core damage frequency

(CDF) per year. The SRA performed a site visit to review Exelons fire model output to

estimate the external risk contributor of the issue. The final risk evaluation estimated the total

(internal and external events risk) increase in CDF to be in the mid E-6/yr range, or of low to

moderate safety significance. The SRA evaluated the internal and external events risk

contribution due to the inoperability of the RCIC system for an assumed 47 day exposure

time.

The analyst used the guidance in the Risk Assessment Standardization Project (RASP)

Handbook, Volume I, Section 2.4, Revision 2.0, to estimate an exposure time using a time

divided by two (t/2) approach. This would represent the time from the last successful

surveillance test divided by two. The approach is appropriate for periodically operated

components that fail due to a degradation mechanism that gradually could affect the

component during the standby period. Given this approach, the internal event contribution

was calculated to estimate the internal event risk increase due to the conditional failure of the

RCIC pump to successfully start. The increase for internal events was estimated at 2.5E-6/yr

increase in CD

F. The dominant sequence involved a loss of condenser heat sink, with

operator action failure to depressurize, and HPCI system failures. The SRA noted from

discussions with Exelon staff that the RCIC system was assumed to be non-recoverable

given the nature of the failure.

To estimate the external risk contribution, the SRA had several discussions and a site visit to

review Exelons preliminary fire model outputs for the conditional failure of the RCIC system

for the 47 days. The 47 days included a conservative additional day for repair time. The SRA

reviewed Exelons fire risk analysis and noted that one of the dominant risk increase

contributors was fire within the 13kV switchgear room. Several other fire areas were

reviewed and the SRA noted that the core damage sequences appeared technically

reasonable given the plant areas and values assumed for mitigating equipment. Exelons

preliminary results showed an increase in external event CDF/yr for the conditional failure of

RCIC for 47 days to be approximately 4.5E-6/yr. The SRA determined the results to be

reasonable.

Exelons model for internal events resulted in an increase in CDF/yr of 1.05E-6/yr which was

considered to compare well with the NRC SPAR model. Exelon performed a review of the

large early release frequency (LERF) impact and determined an overall increase in LERF due

to both external and internal events for the RCIC failure for 47 days to be a nominal 6E-8/yr.

Therefore, the SRA review of the dominant sequences and Exelons LERF results affirmed

that LERF did not increase the risk over that determined from the increase in CDF.

Basis for Discretion: The inspectors determined that the maintenance strategy for these

switches was consistent with requirements and standards that existed at the time and that

there was no relevant operating experience that would have reasonably necessitated

consideration of additional maintenance actions. As a result, no performance deficiency was

identified.

The inspectors assessment considered:

The industry, regulatory, and Exelon service life standards were reviewed for static O-

ring pressure switches. Exelons assessment of the pressure switch service condition

(critical, mild conditions, low-duty cycle) required a preventive maintenance task to

perform periodic calibration and to replace the switch as-required. There was no

time-based replacement task prescribed by any standard for this switch. The

inspectors determined that Exelons assessment was adequate and the corresponding

preventive maintenance activities met applicable standards.

The subject pressure switch was installed during original construction and the

calibration results of the pressure switch had been satisfactory from 2003 until the

2018 failure. The inspectors reviewed the maintenance and calibration history on the

pressure switch and did not identify any adverse trends or conditions adverse to

quality that would have required further evaluation or replacement of the pressure

switch.

Industry operating experience information available to Exelon did not identify the

potential for the age-related failure mode of the pressure switch o-ring and diaphragm

that occurred at Peach Bottom.

The NRC determined that it was not reasonable for Exelon to have been able to foresee and

prevent this violation of NRC requirements, and as such, no performance deficiency existed.

Therefore, the NRC has decided to exercise enforcement discretion in accordance with

Sections 2.2.4 and 3.10 of the NRC Enforcement Policy and refrain from issuing enforcement

action for the violation of TSs (EA-18-108). Further, because Exelons actions did not

contribute to this violation, it will not be considered in the assessment process or the NRC

Action Matrix.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On October 23, 2018, the inspectors presented the quarterly resident inspector inspection

results to Mr. Pat Navin, Peach Bottom Site Vice President, and other members of the Exelon

staff.

DOCUMENTS REVIEWED

71111.05Q

Procedures

PF-78H, Revision 9, Turbine Building Common, Cable Spreading and Computer Rooms -

Elevation 150-0

PF-117, Revision 10, Unit 3 Turbine Building, Emergency Battery Switchgear Rooms -

Elevation 135-0

PF-127, Revision 10, Unit 2 Turbine Building, Emergency Battery Switchgear Rooms -

Elevation 135-0

71111.11

Procedures

DD-20, Revision 1, Operations Department Description

OP-AA-1, Revision 1, Conduct of Operations

OP-AA-100, Revision 0, Description of the Exelon Nuclear Conduct of Operations Manual

OP-AA-20, Revision 0, Conduct of Operations Process Description

Miscellaneous

Appendix H, Generic Licensed Operator Observation Checklists

71111.13

Procedures

ST-I-01G-100-2, Revision 7, ADS Channel A Logic System Functional test

WC-AA-104, Revision 28, Integrated Risk Management

WC-AA-104-F-01, Revision 0, Risk Screening / Mitigation Plan

Miscellaneous

DBD No. P-S-31, Revision 4, ADS

71111.19

Procedures

RT-M-40H-925-3, Revision 7, HPSW/ESW Pump Room Ventilation Logic System Functional

Test

WOs

04705247-03 04705247-04

71111.22

Procedures

HU-AA-1211-F-01, Revision 4, Pre-Job Briefing Checklist

OP-AA-101-111-1001, Revision 20, WRO Work Release Checklist

RT-O-052-750-2, Revision 10, E-2 Diesel Alternative Shutdown Control Functional

SI3P-7-9102-B1C2, Revision 8, Calibration Check of Drywell Pressure Instruments PT/PR

9102B and Backup Nitrogen Supply to ADS Pressure Instruments PT/PS/DPS 9142B

ST-O-052-202-2, Revision 22, E-2 Diesel Generator Slow Start and Full Load Test

71124.07

Procedures

CY-AA-130-201, Revision 006, Radiochemistry Quality Control

CY-AA-170-1100, Revision 004, Quality Assurance for Radiological Monitoring Programs

QA-ES-200, Revision 001 EIS Quality Assurance Program Manual - Technical Services

K-QAM-1, QA Manual, Teledyne Brown Engineering Environmental Services, Revision 32

Issue Reports

04164092

Documents:

ODCM, Revision 016, Offsite Dose Calculation Manual, 12/21/2017

NEI 07-07 Peer Assessment Report 2016

2017 Annual Radiological Environmental Operating Report 75

71152

Procedures

COL 23.1.A-3, Revision 24, HPCI System

M-C-750-001, Revision 22, RCIC Turbine Major Inspection

M-C-756-001, Revision 33, HPCI Turbine Inspection

OP-AA-108-115, Revision 21, Operability Determinations

PI-AA-120, Revision 8, Issue Identification and Screening Process

PI-AA-125, Revision 6, CAP Procedure

RRC 13.1-2, Revision 4, RCIC System Operation during a Plant Event

RRC 23.1-3, Revision 6, HPCI System Operation during a Plant Event

RT-O-023-302-3, Revision 25, HPCI Turbine Overspeed Trip Reset Time Check/Adjustment

and HPCI Auxiliary Oil Pump and Manual Trip Lever Tension Test

RT-I-094-800-2, Revision 4, Reactor Building Ambient Temperature Data Collection

SO 13.1.A-3, Revision 15, RCIC System Alignment for Automatic or Manual

SO 23.1.A-3, Revision 24, HPCI System Setup for Automatic or Manual Operation

SO 23.1.B-3, Revision 22, HPCI System Manual Operation

Completed Surveillance Tests, Functional Tests, and Post-Modification Tests

ST-I-023-100-2, HPCI Logic System Functional Test, performed 5/2/18

ST-I-023-100-3, HPCI Logic System Functional Test, performed 4/21/16

ST-O-023-300-2, HPCI Pump, Valve, Flow and Unit Cooler Functional and In-Service Test

without Vibration Data Collection, performed 6/7/18

ST-O-023-300-3, HPCI Pump, Valve, Flow and Unit Cooler Functional and In-Service Test

without Vibration Data Collection, performed 6/28/18

Issue Reports

03997737 0966085 2418959 2625671 2722895 3961408

4001946 4004135 4005532 4005664 4020045 4033575

4054013 4054022 4055480 4055985 4059811 4067994

4086666 4088214 4095900 4095901 4096366 4098271

4098695 4099040 4114591 4146368 4114824 4114847

24240 4129583 4151091 4153864 4163279 4165993*

4166046* 4195491 4306865 4692435 4692438 4749239

  • IR written as a result of this inspection

Drawings

280-A-10, Revision 22, Floor Plan 91-6

M-1-J-6 Sh. 1, Revision 6, Outline HPCI Pump Drives

Miscellaneous

11187-2204, Revision 17, Pipe Break Outside Containment HELB Compartment Analysis

4004135-04, Revision 0 and 1, MO-3-23-014 (HPCI Turbine Steam Supply Valve) Steam

Leak-by Monitoring Adverse Condition Monitoring and Contingency Plan

4096366-02, Revision 0, MO-2-23-014 (HPCI Turbine Steam Supply Valve) Steam Leak-by

Monitoring Adverse Condition Monitoring and Contingency Plan

EQ-PB-026, Revision 0, Static O-Ring Pressure Switch, dated 8/26/2014

Franklin Institute Research Laboratory Report F-A5653-6, Environmental Qualification Testing

of Class 1E Equipment SOR Pressure Switch 5N-AA3 Peach Bottom Atomic Power

Station, Units 2 and 3, dated 1/17/1984

NE-00164, Revision 6, Specification for Environmental Service Conditions Peach Bottom

Atomic Power Station Units 2 and 3

NRC Information Notice 94-84: Air Entrainment in Terry Turbine Lubricating Oil Systems,

dated 12/2/94

OBSR 2017-184971, Engineering Event Free Clock Reset Communication, dated 10/11/17

PM-0785, Revision 6D, Power Rerate Evaluation - LOCA/High Energy Line Break Analysis

Unit 2 Room 8 Temperature Data from October 1995 through July 2018

System Health Reports, System Walkdowns, & Trending

20P033 OL1 & OL2 Pump Bearing Lube Oil Sample Analysis Results, 5/3/17 - 6/7/18

20P036 OL1 & OL2 Pump Bearing Lube Oil Sample Analysis Results, 6/18/17 - 7/28/18

20P038 Gearbox Lube Oil Sample Analysis Results, 5/3/17 - 6/7/18

20S037 Pump (Sump) Lube Oil Sample Analysis Results, 5/3/17 - 6/7/18

20S038 OL1 Bearing Lube Oil Sample Analysis Results, 6/18/17 - 7/28/18

30P033 OL1 & OL2 Pump Bearing Lube Oil Sample Analysis Results, 6/21/17 - 6/28/18

30P036 OL1 & OL2 Pump Bearing Lube Oil Sample Analysis Results, 4/11/17 - 7/24/18

30P038 Gearbox Lube Oil Sample Analysis Results, 6/21/17 - 6/28/18

30S037 Pump (Sump) Lube Oil Sample Analysis Results, 9/20/17 - 6/28/18

30S038 OL1 Bearing Lube Oil Sample Analysis Results, 4/11/17 - 7/24/18

U2 HPCI ACMP IR 4096366 Lube Oil Sump Sample Results, 1/26/18 - 8/11/18

U3 HPCI ACMP IR 4004135 Lube Oil Sump Sample Results, 3/24/17 - 10/22/17

Unit 2 and Unit 3 High Pressure Injection (RCIC & HPCI) System Health Report, dated 8/1/18

Unit 2 and Unit 3 HPCI Turbine Temperature Trends, April 2017 - July 2018

Technical Evaluations

EC 621770

EC 624540

Vendor Manuals

M-1-JJ-30, Revision 9, HPCI Terry Turbine Manual

VPF 2059-44-2, RCIC Turbine Manual, March 1972

71153

Procedures

AD-AA-101-1002, Attachment 1, Revision 1, Procedure Approval Form

ER-AA-520, Revision 1, Instrument Performance Trending

FF-01, Revision 23, Fire Brigade

IC-11-00001, Revision 3, Calibration of Plant Instrumentation and Equipment

IC-C-11-00010, Revision 2, Calibration of Pressure and Vacuum Switches

M-052-002, Revision 42, Diesel Engine Maintenance

M-052-006, Revision 18, Diesel Run After Major Overhaul

PF-132, Revision 9, Diesel Generator Building, General Area - Elevation 127-0

PI-AA-120, Revision 8, Issue Identification and Screening Process

PI-AA-125-1003, Revision 4, RCIC Turbine Trip on Startup

RT-O-052-253-2, Revision 39, E-3 Diesel Generator Inspection Post-Maintenance Functional

Test

SI3P-13-72-ABCE, Revision 7, Calibration Check of RCIC Pump and Turbine Pressure

Switches PS 3-13-67-1 and PS 3-13-72A/B

SO 52A.8.C, Revision 43, Diesel Generator Running Inspection

ST-O-013-3, Revision 12, RCIC Pump, Valve, Flow and Unit Cooler Functional and In-Service

Test without Vibration Data Collection

ST-O-052-313-2, Revision 21, E-3 Diesel Generator Slow Start Full Load and IST Test

ST-O-052-414-2, Revision 26, E-4 Diesel Generator Fast Start and Full Load Test

TQ-AA-223-F050, Revision 0, Nuclear Generating Station Instrument Maintenance

Initial Training Program

TQ-AA-223-F050, Revision 14, Nuclear Generating Station Instrument Maintenance

Training Program

WC-AA-111, Revision 5, Surveillance Program Requirements

Drawings

280-M-359, Sheet 2, Revision 48, RCIC System

280-M-360, Sheet 2, Revision 54, RCIC Pump Turbine Details

Issue Reports

0446457 3960207 3992819 4054092 4129583

29691 4146368 4146926 4149044 4155919

4166846

Miscellaneous

DBD No. P-S-07, Revision 18, Diesel Generator and Auxiliary Systems

EPRI, Service Life Assessment Guide, An Aging Assessment Reliability Process,

2016 Technical Report

SRS A-5, Revision 0, EQ Supplemental Review Sheet (SRS)

Fairbanks Morse, Inlet Air Check Valve Lubrication, Service Information Letter, Dated

February 18, 1985

Information Notice No. 87-16: Degradation of Static O-Ring Pressure Switches, In 87-16,

Dated April 2, 1987

LER 2-18-002, EDG Air Inlet Check Valve Failure Results in a Condition Prohibited by TSs

LER 3-18-001, RCIC System Pressure Switch Failure Results in Condition Prohibited by TSs

Lube Oil Flushing Procedure

PBAPS PORC Agenda, dated June 21, 2018PEA-98441, Failure Analysis of a Pressure Switch

Manufacturer: Static-O-Ring (SOR, Inc.)

Model 6N-AA3, dated May 30, 2018e

PEA MRC Agenda for July 2, 2018

Work Orders

618948

E-3 EMERGENCY DIESEL GENERATOR FAILURE DETAILED RISK EVALUATION

Conclusion:

The total increase in core damage frequency (CDF) for the performance deficiency related to

the degraded E-3 emergency diesel generator (EDG) turbochargers was estimated to be

Preliminary White, a finding of low to moderate safety significance. The calculated conditional

risk increase is dependent on the assumed exposure time, assumption of EDG failure, credit

considered for FLEX implementation and is dominated by external events such as postulated

fires within both Units 4kV switchgear rooms. Based on an initial best estimate assumption that

the degraded condition would fail the function of the E-3 EDG, the assumed exposure time, and

consideration of risk mitigation provided by FLEX strategies using sensitivity analyses, the

increase in CDF/yr was determined to be within the range of 4.5E-6/yr to 6E-6/yr for Unit 2, and

5.6E-6/yr to 8.5E-6/yr for Unit 3.

Influential Assumptions

This review consisted of determining the best estimate risk increase for the internal and external

postulated events for Unit 2 and Unit 3. This required various key assumptions for this

determination including the following:

EDG Functionality and Common Cause Failure

The failure probability for the Standardized Plant Analysis Risk (SPAR) model basic event

for the E-3 EDG, EPS-DGN-FR-DGC, was changed to TRUE, to represent the failure and to

account for the increased potential for common cause failure of the remaining EDGs. An

increased common cause failure probability is used based upon the performance deficiency

described in this report, which when viewed in a broader context could have resulted in a

failure of other EDGs. This assumption is consistent with guidance in Risk Assessment

Standardization Project (RASP) Volume 1, Section 5.

Exposure Time

Exposure time for the failed E-3 EDG was established at 196 days. The analyst used the

RASP Volume I guidance, Section 2.5, for a run time component failure. This approach is

appropriate for standby operated components that fail due to a degradation mechanism that

affects the component during its operation, since this was a vibration induced failure.

Per this guidance, the exposure time starts when the component no longer had the

capability to operate for the probabilistic risk assessment (PRA) mission time (i.e. 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />).

The analyst reviewed E-3 EDG surveillance test results and added up the run time hours to

determine when the EDG had proven a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> run time period. The results of this review

showed that in early December 2017, the EDG had over a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> proven run time and

therefore the exposure time was taken from that time until the failed test on June 13, 2018.

This period amounted to a best estimate exposure time of 186 days. Additionally, the E-3

EDG was out of service for repairs for an additional 10 days, which would amount to a total

exposure time due to this performance deficiency of 196 days.

In this case, two degraded conditions existed including an inadequate check valve shaft to

disk interference fit, which would result in higher vibration of the shaft and disk at any loads,

and a hydraulic dashpot which was not kept filled with oil. The dashpot assembly provides

some resistance against the valve opening and controls the rate of valve motion as it opens

or closes. It also dampens out oscillations caused by changes in air flow, engine load, and

anything else that could change the air flow pattern through the valve. Discussions with

Exelon personnel indicated that even at low EDG loads with the check valve to the

turbocharger not yet open there is vibration visually observed on the shaft mechanism which

is induced by EDG operation. The analyst noted that with the dashpot not filled, there would

be less dampening effect in the closed position and with the shaft not fit to the disc (design

is an interference fit), this would increase the stress on the pin connecting the shaft and inlet

check valve (disc) even at low loads and EDG startup. Additionally, the analyst noted that

during the failed surveillance test, the time period that the machine was near the estimated

2500 kW check valve opening load was of a very short duration (i.e. minutes). Because the

operator did not hear any issues with the machine for up to at least 20 minutes after full load

conditions were met (2750kW area), it is uncertain when exactly the pin failed as it would

likely not take very long for this pin to cause the damage that was observed with the

turbochargers rotating at speeds of 16,000 rpm. In summary, the E-3 EDG was verified to

be in the range of load equivalent to the estimated initial opening of the check valve for a

very short duration of time, which creates uncertainty when the pin would have failed due to

an overall vibration mechanism and it may have failed once it reached full load conditions.

The analyst noted that Exelons assessment of the direct cause of the failure within

Licensee Event Report (LER) 05000277/2018-002-0 was reasonable and the LER indicated

that several causal factors existed, including shaft bushing wear and inadequate shaft to

disk fit, which resulted in higher vibration of the shaft and disk. With the higher vibration,

tolerances for the interference fit of the pin to the disk shaft were not adequate to prevent

the pin from becoming dislodged. The analyst noted that vibration would exist at various

unknown levels due to the degraded condition from low load throughout loads above the

continuous rating of the E-3 EDG. There was no evidence that vibration for this degraded

condition would not have existed internal to the check valve throughout a spectrum of EDG

loading. Lastly, the analyst noted that during an actual loss of offsite power (LOOP) event,

loading can and will vary as operators start and remove equipment in response to plant

conditions. For instance, the analyst observed in a simulator demonstration that when

residual heat removal (RHR) was placed in service at designated allowed flowrate the

loading on the E-3 EDG was a nominal 3000 k

W. However, when RHR flowrate was

reduced to the lower limits allowed within procedural guidelines, the load on the E-3 EDG

dropped to just below 2600 kW. Loading changes such as this would be anticipated during

actual events and changes on the check valve demand and positioning would not be

unexpected.

Standardized Plant Analysis Risk (SPAR) Model Changes and Sensitivity Analyses

A further detailed review of the NRC Peach Bottom SPAR model outputs resulted in identifying

several conservatisms. The SPAR model was modified to include FLEX modifications, which

the station had developed in response to NRC Order 12-049, Order to Modify Licenses with

Regard to Requirements for Mitigation Strategies for Beyond-Design-Basis External Events

(ML12054A735), and affected how the units would respond to an extended loss of alternating

current power. The plant-specific modifications that were included in the revised model were

described in Exelons Overall Final Integrated Plan (ML13059A305). Additionally, the analyst

determined that a second conservative modeling issue existed. Specifically, for postulated

recirculation pump seal failures, the reactor core isolation cooling (RCIC) system was not being

credited as capable of makeup for the postulated leak, which the analyst determined would

likely be well below the capability of the RCIC system. Therefore, through discussions with INL

personnel, a revised version of the model was developed in order to more accurately model the

change in risk due to this performance deficiency.

The analyst noted the Peach Bottom Unit 2 NRC SPAR model had much more detail

incorporated for external hazard events than the Unit 3 model and therefore used Unit 2 as a

surrogate for the determination of the increase in CDF due to the finding. The E-3 EDG referred

to in this evaluation is referred to in the SPAR model as the C EDG in the following

discussions.

Because of the nature of this particular failure of an EDG, the postulated events of importance

become associated with scenarios where alternative offsite alternate current (AC) power

sources are not available. As noted, one of the major plant modifications made within the last

few years, is an extensive change to the strategies of how to handle situations where there is, in

part, a complete loss of alternating current to the safety busses. FLEX or mitigating strategies

have been developed to provide additional protection for scenarios where it is not expected an

AC source can be readily recovered. Therefore, changes to the SPAR model were required to

ensure that the model matched the reality of the plant and procedures. This was incorporated

through a revision provided by INL SPAR model experts, and was revised by the analyst

through the knowledge of how the FLEX strategy would be implemented. In this way, some

amount of appropriate credit is recognized. It is, however, recognized that equipment used is

often portable with limited reliability data available to-date. Also, there are operator actions

required to achieve success. Therefore, uncertainty was considered by providing various

changes in assumptions for FLEX equipment failure rates through different sensitivity

evaluations. In this way, the impact of varying these assumptions could be observed and a

reasonable bounding approach could be achieved. Notwithstanding this, by using different

assumptions through a spectrum of failure rates this provides information to use a best estimate

risk informed evaluation of this degraded condition.

This revised model was then used to assess the internal events contribution to risk from this

degraded condition. Additionally, through discussions with Exelon staff, it was recognized that

several revisions were made to the Peach Bottom external event fire model. Therefore, the

existing Unit 2 SPAR model version 8.50 for fire external events was not used in the calculation

of external fire risk and the licensees fire model results were reviewed and considered. The

analyst reviewed a sample of core damage cutsets with Exelon personnel and determined them

to represent technically justified scenarios through a review of specific fire areas and the logic of

impact on applicable equipment.

The SPAR model for external events such as seismic and high wind did appear to have

appropriate core damage cutsets and therefore was used to evaluate other external events.

The revised SPAR model which incorporated FLEX strategies was linked to the seismic and

high wind event trees to ensure that FLEX would be credited as appropriate. Therefore, the

NRC SPAR model was used to develop a best estimate risk increase for internal events and for

postulated seismic and high wind external events.

Because there is very little data associated with portable type FLEX equipment, several different

sensitivities were performed using different values for FLEX equipment reliability to see what

impact this would have on the overall risk contribution for the failed EDG. Several different

cases were run which varied the FLEX equipment failure probabilities to gain an understanding

of the impact on the overall risk contribution. This was performed for both the external events

(Fire, Seismic, High Wind) and internal events. This included a spectrum of values including the

use of Exelons initial preliminary values for FLEX equipment reliability along with several

different cases such as increasing the fail to start (FTS) by a factor of 2 and the fail to run (FTR)

by a factor of 2, along with a case where the FTS was increased by over an order of magnitude

and the FTR was increased by a factor of 2. Lastly, a case considered bounding and likely

conservative was run for fire which used FLEX equipment failure rates of 0.1.

Per discussions with Exelon staff, for the development of the FLEX equipment reliability data

used in the Peach Bottom internal events and fire PRA models, no plant specific data was

collected or used. The Peach Bottom models use plant specific data gathered through

December 31, 2013, when applicable; however, data gathering for Peach Bottom FLEX

equipment did not begin until 2016. Therefore equipment failure probabilities for Exelons initial

BASE case are based on the 2015 version of NUREG/CR-6928 data. Exelon recognized that

equipment used as part of the FLEX strategies includes portable equipment such as FLEX

pumps and FLEX diesel generators (DGs). Therefore, they had performed initial sensitivity

assessments where the random failure probabilities of portable equipment, which lacks specific

data, is estimated as double those of similar permanently installed components.

LICENSEE BASE CASE per discussion (BC) FLEX failure probabilities

FLEX DG FTS 6.6E-3

FLEX DG FTR for 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> 3.65E-2

FLEX diesel driven (DD) makeup pump FTS 3.15E-3

FLEX DD makeup pump FTR 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> 4.75E-2

SENSITIVITY 1 - basecase failure probabilities doubled (2x sensitivity) used for internal events

FLEX DG FTS 1.32E-2

FLEX DG FTR for 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> 7.3E-2

FLEX DD makeup pump FTS 6.3E-3

FLEX DD makeup pump FTR 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> 9.5E-2

SENSITIVITY 2 - Used for fire results *

FLEX DG FTS 7E-2

FLEX DG FTR for 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> 7.3E-2

FLEX DD makeup pump FTS 7E-2

FLEX DD makeup pump FTR 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> 9.5E-2

  • used double Licensee base case FTR, increased FTS to 7E-2, values used for fire only

SENSITIVITY 2 - Used for internal events/seismic/high wind SPAR model runs *

FLEX DG FTS 7E-2

FLEX DG FTR for 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> 9E-2

FLEX DD makeup pump FTS 7E-2

FLEX DD makeup pump FTR 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> 9E-2

  • based the 7E-2 on a failure noted for a DD makeup pump in a review of actual plant data, used

similar FTR probability with difference insignificant to final results

SENSITIVITY 3 - Used only for fire external events

FLEX DG FTS 0.1

FLEX DG FTR for 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> 0.1

FLEX DD makeup pump FTS 0.1

FLEX DD makeup pump FTR 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> 0.1

Internal Event Conditional Risk

Internal events were not a dominant contributor to risk and therefore only two sensitivities were

run. Sensitivity 1 and Sensitivity 2 were run to explore the changes in CDF increase given

different assumed FLEX equipment failure rates.

Sensitivity 2 - Internal (Slightly higher order of magnitude FTS and higher FTR)

A change set was developed to change the FLEX equipment failure rates including the FLEX

operator action failure probabilities for FLX-XHE-XM-480 and FLX-XHE-XM-RPV to a value of

0.1. This would factor in the potential impact of dependency related to multiple operator action

failures within a core damage sequence. A condition case change set was then developed

using the above conditions along with setting the EPS-DGN-FR-DGC to TRUE as the

conditional case.

The base case was 5.5E-6/yr and the conditional case was 6.83E-6/yr.

The increase in CDF was therefore 1.33E-6/yr x (196 days/365 days) = 7.2E-7/yr.

The dominant cutsets were as follows:

LOOP weather related, operator failure to establish Conowingo tie line setup, failure of

the E-2 EDG to run, failure to recover an EDG, failure to cross tie emergency busses,

failure to recover offsite power, convolution factor, and a failure of RCI

C.

LOOP weather related, operator failure to establish Conowingo tie line setup, the E-2

EDG fails to run, failure to recover an EDG, failure to cross tie emergency busses, failure

to recover offsite power, a convolution factor, and failure to stage or run or load the 480V

portable FLEX DG.

Sensitivity 1 - Failure rates of 2x or double the NUREG/CR 6928 data

The same method was employed to develop change sets for the base case and conditional

case altering the FLEX equipment failure rates and failing the E-3 EDG FTR in the conditional

case.

The base case was 5.5E-6/yr and the conditional case was 6.67E-6/yr.

The increase in CDF was therefore 1.17E-6/yr x (196/365) =6.3E-7/yr

Several examples of dominant cutsets are as follows:

LOOP grid related, failure to establish Conowingo tie line, E-2 EDG out for test and

maintenance, failure to recover EDG, failure to cross tie emergency busses, failure to

recover offsite power, and RCIC failure

LOOP grid related, failure to establish Conowingo tie line, E-2 EDG out for test and

maintenance, failure to recover an EDG, failure to cross tie emergency busses, failure to

recover offsite power, and failure to stage or run or supply a FLEX reactor pressure

vessel pump.

Fire External Event Conditional Risk

It was determined that fire risk was the dominant contributor to risk. This was true for both the

impact on Unit 2 and Unit 3 with a slightly higher increase in CDF/yr for Unit 3. The areas of

importance from a fire perspective were related to the switchgear rooms.

Both of the Unit 2 and Unit 3 fire areas which dominated the conditional increase in risk were

associated with the 4kV switchgear rooms and contributed over 80% for each unit of the risk

contribution.

FLEX sensitivities were varied and more important for the external fire events. These were

applied to evaluate the impact of the varying assumptions for the reliability of the FLEX

equipment. The impact of the various equipment failure rate sensitivities was analyzed.

The analyst noted that the operator actions to gain access to, deploy, hook up, and start the

equipment was typically given a value of 0.1 for the human error probability by the licensee for

the fire scenarios. This was consistent with a SPAR-H human error probability calculation with

performance shaping factors of barely adequate time, high stress, moderately complex, and

nominal training and procedures. Additionally, factoring in the potential for low dependency

given this could be the second operator failure action in a cutset would result in a value close to

0.1. Therefore the analyst determined this was a reasonable value to go along with the various

sensitivities associated with the equipment as well.

Sensitivity 3 - Increasing FLEX equipment failure probability to 0.1

Unit 2 fire risk increase in CDF given E-3 FTR

9.1E-6/yr x exposure time (196 days/365 days) = 4.9E-6/yr increase in CDF/yr

Unit 3 fire risk increase in CDF given E-3 FTR

1.4E-5/yr x (196/365) = 7.5E-6/yr increase in CDF/yr

The analyst considered this to be a reasonable best estimate for a bounding assessment given

the high failure rates assumed which exceed actual failure rates to date at the station observed

with the limited data set.

Sensitivity 2 - Increasing FLEX equipment FTS over order magnitude and 2x baseline FTR

Unit 2 fire risk increase in CDF given E-3 FTR

8.19E-6/yr x 196/365) = 4.4E-6/yr increase in CDF/yr

Unit 3 fire risk increase in CDF given E-3 FTR

1.25E-5/yr x 196/365 = 6.7E-6/yr increase in CDF/yr

Licensee Base Case per discussion (Using NUREG/CR-6928 data 2015 version)

Unit 2 fire risk increase in CDF given E-3 FTR

6.5E-6/yr x 196/365 = 3.5E-6/yr increase in CDF/yr

Unit 3 fire risk increase in CDF given E-3 FTR

8.5E-6/yr x 196/365 = 4.6E-6/yr increase in CDF/yr

The analyst considered Sensitivity 2 to likely be more representative of the actual failure rates

given the limited data to date, however more importantly, the analyst considered the three

sensitivities above to be in agreement with the best estimate overall risk estimate of a White

issue or of low to moderate risk significance.

Dominant Fire Areas

Several of the dominant fire areas were as follows:

Unit 2

An area which contributed a nominal 30% of the risk increase was associated with fire area 35

(E23 4kV Switchgear Room). The significant contributor or event were electrical/high energy

arc faults (HEAFs), fires involving 4kV Bus Duct 00A20 or the E23 4kV Switchgear. The top

core damage cutsets involved the fire scenario initiating event, the operator failure to perform

the 4kV EDG backfeed, and the operator errors associated with aligning the FLEX generator

and performing a deep direct current (DC) load shed to extend battery life to support alignment

of the FLEX generator.

A second area contributing at least 15% of the total fire risk was associated with the E12 4kV

Switchgear Room. The contributing events were associated with electrical/HEAF fires involving

the 4kV Bus Duct 00A19 and the E12 4kV Switchgear.

The significant core damage cutsets involved fire scenario HEAFs at E12 and 00A19 along with

common cause failure of the E-1 and E-4 or E-2 and E-4 EDGs. Additional core damage

cutsets involve the same initiating events with random failure of the E-2 and either failure of the

operator action to perform 4kV backfeed or failure of the E-4 DG. The analyst noted that Exelon

appropriately had not credited FLEX in these cutsets as the fires damage division 1 equipment

that disables the use of FLEX phase 1 equipment.

The analyst noted that through a review of fire related cutsets it was evident that Exelon

appropriately modeled the loss of FLEX capability when the RCIC system was impacted or

equipment significant to the FLEX implementation strategy was affected.

Unit 3

An area that contributed at least 33% of the total fire risk was associated with fire scenarios

within the E23 4kV Switchgear Room. Some of the events consisted of electrical/HEAF fires

involving 4kV bus duct 00A20 or the E23 4kV Switchgear. The top core damage cutsets involve

the fire scenario initiating event, the operator action failure to perform the 4kV EDG backfeed,

and the operator action failures associated with aligning the FLEX generator or performing a

deep DC load-shed to extend battery life to support alignment of the FLEX generator.

Another dominant fire area was associated with fires in the E22 4kV Switchgear Room. The

events consisted of electrical/HEAF fires involving 4kV bus duct 00A20 or the E22 4kV

Switchgear. The top core damage cutsets involve the fire scenario initiating event, the failure to

perform the 4kV EDG backfeed, and the failures associated with aligning the FLEX generator or

performing a deep DC load-shed to extend battery life to support alignment of the FLEX

generator.

Other External Event Risk Contribution

The following external events, High Wind and Seismic, were calculated using the SPAR Unit 2

model. A comparison of model runs, indicated that both units were very similar in nature and

therefore the runs for the Unit 2 model will be considered identical contributions for Unit 3 for

these events.

High Wind 90 mph

Sensitivity 2 - Slightly higher order of magnitude FTS and higher FTR Internal events

A change set was developed to change the FLEX equipment failure rates including the FLEX

operator action failure probabilities for FLX-XHE-XM-480 and FLX-XHE-XM-RPV to a value of

0.1. This would factor in low dependency as a second error in a sequence. A condition case

change set was then developed using the above conditions along with setting the EPS-DGN-

FR-DGC to TRUE as the conditional case.

The base case was 7.6E-8/yr and condition case was 2.58E-7/yr

The increase in risk was therefore 1.82E-7/yr x 196/365 = 9.5E-8/yr or on the order of 1E-7/yr.

The dominant cutset was events with high winds, failure to establish the Conowingo tie line, the

E-2 EDG in test and maintenance, failure to recover an EDG, failure to crosstie the emergency

buses, a conditional LOOP given the wind 0.5, operator failure to recover offsite power, and

RCIC failure.

Sensitivity 1 - Failure rates of 2x or double the Licensee NUREG/CR numbers

The same method was employed to develop change sets for the base case and conditional

case altering the FLEX equipment failure rates and failing the E-3 EDG FTR in the conditional

case.

The base case was 7.55E-8/yr and the conditional case was 2.36E-7/yr

The increase in risk was therefore 1.6E-7/yr x 196/365 = 8.5E-8/yr

The dominant cutset was similar to the above case.

Seismic Events

The final external event evaluated were the Seismic events which fell into 5 bins relative to the

strength of the seismic event.

For this case a base case and conditional case was run, then the cutsets for each were

gathered into the core damage seismic end state to ensure that they were not being double

counted.

Sensitivity 2 - Order of magnitude approximately for FTS and 2x or double FTR)

The base case for the gathered cutsets was 1.62E-5/yr and the condition case was 1.68E-5/yr.

The increase in risk was 6E-7/yr x 196/365 = 3.2E-7/yr

Several dominant cutsets were a seismic event in bin 3 (0.5-0.75g) with a LOOP, FTR of the

E-2 EDG, and a seismic induced small break loss-of-coolant-accident or a failure of the RCIC

lube oil cooler or a failure of the FLEX generator.

Sensitivity 1 - Failure rates of 2x or double the Licensee NUREG/CR numbers

The change in risk between the base case and conditional case was

5.7E-7/yr x 196/365 = 3.1E-7/yr

The dominant cutsets were a bin 3 seismic event, with a LOOP, and failure of E-2 EDG to run

and failure to deploy/start the FLEX DD makeup pump.

Large Early Release Frequency

The analyst reviewed portions of the Peach Bottom PRA summary notebook relative to the

analysis of large early release frequency (LERF). The licensee evaluated a Level 2

methodology analyzing issues such as magnitude and timing of calculated radionuclide releases

through level 2 containment event trees. The analyst noted that the Licensee had used a LERF

multiplier for both units relative to the CDF sequences of a nominal 5E-2. Therefore, this does

not increase the LERF importance with respect to risk over or beyond that calculated for the

CDF/yr increase.

A bounding result was associated with Unit 3 (Sensitivity 3 for FLEX) for the conditional change

in LERF and was a 4.3E-7/yr annualized increase in risk due to the degraded E-3 EDG. This

would result in 4.3E-7/yr x 196 days/365 days = 2.3E-7/yr increase in LERF due to the

condition. This bounds any LERF contribution from internal events and therefore the best

estimate of risk is represented by the estimated increase in total CDF/yr for the condition.

For LERF, per Inspection Manual Chapter 0609, Appendix H, Table 5.2, LERF factors of 1.0

and 0.6 are used for high pressure core damage accident sequences with the drywell dry or

flooded, respectively. These Appendix H LERF factors are considered conservative bounding

values. More recent insights from an NRC Office of Research sponsored study by Energy

Research, Inc. (ERI/NRC-03-04), November 2003 and subsequent State of the Art Reactor

Consequence Analysis Project at Peach Bottom Nuclear Power Station (NUREG/CR-7110)

have identified that improved modeling and analysis of anticipated types and sizes of reactor

coolant ruptures, projected containment heating and fuel-coolant interactions, and operator

actions taken to flood containment in accordance with Severe Accident Management

Guidelines, significantly reduce the potential for containment breach and the likelihood of a

LER

F. Furthermore, the dominant sequences discussed throughout this review would result in

considerable time (estimated 8-10 hours) before postulated core damage and an a potential

additional 8-10 hours until containment breach. Therefore, the above reports indicate a more

benign containment response at the time of vessel breach, in terms of direct containment

heating and fuel-coolant interaction-induced containment failure. Therefore, the analyst

determined Exelons LERF evaluation to be reasonable.

Model comparisons and Licensee Risk Preliminary Methodology

Exelons internal events analysis for the conditional failure of the E-3 when evaluated for a 196

day exposure time by the analyst was found to be very similar with regard to the calculation of

the contribution of the increase in CDF/yr for internal events (i.e. nominal 5E-7/yr). This gives

added confidence that the NRC SPAR model and the licensees internal events model were

reasonably aligned in the assessment of the issue.

Per discussions with Exelon PRA personnel, it is believed that FLEX should be credited in any

scenario where there is the complete loss of AC power, except for conditions where RCIC is

impacted which is the phase I strategy for FLEX. The analyst determined this to be a

reasonable conclusion and recognized through a review of various fire scenario cutsets, that

FLEX credit was appropriately not being considered for cases which impacted the FLEX

procedures and strategy.

Preliminary Conditional Risk Increase Calculation CDF/yr

Total Risk Internal + External Events

Using the lower FLEX failure rates of sensitivity analysis

Unit 2

Fire 3.5E-6/yr + Internal 6.3E-7/yr + High Wind 8.5E-8/yr + Seismic 3.2E-7/yr = 4.5E-6/yr

Unit 3

Fire 4.6E-6/yr + Internal 6.3E-7/yr + High Wind 8.5E-8/yr + Seismic 3.2E-7/yr = 5.6E-6/yr

Higher FLEX failure rates of sensitivity analysis

Unit 2

Fire 4.9E-6/yr + Internal 7.2E-7/yr + High Wind 9.5E-8/yr + Seismic 3.2E-7/yr = 6E-6/yr

Unit 3

Fire 7.5E-6/yr + Internal 7.2E-7/yr + High Wind 9.5E-8/yr + Seismic 3.2E-7/yr = 8.5E-6/yr

Therefore, the analyst noted that the increase in CDF/yr for the failure of the E-3 EDG was

within the range of 4.5E-6/yr to 6E-6/yr for Unit 2 and 5.6E-6/yr to 8.5E-6/yr for Unit 3.

This would represent a Preliminary White issue or of low to moderate safety significance for the

conditional failure of the E-3 EDG for both Unit 2 and Unit 3.

Qualitative Considerations

As noted, FLEX was not initially incorporated into the SPAR model. This was recognized and a

modification was made to the appropriate Unit 2 Peach Bottom SPAR model (used as a

surrogate for Unit 3 also) to appropriately consider risk reduction for FLEX strategies.

A sensitivity was run for the potential effect of a reduction in risk going backwards crediting run

time of the E-3 EDG over the 186 days prior to failure. This would result in some additional time

for recovery of offsite power. This sensitivity evaluation showed an insignificant change to the

overall risk conclusions and does not apply to the dominant risk contributor or fire scenarios.

It should also be noted that actual postulated LOOP scenarios would result in the E-3 EDG

loading being different in that the loads on the EDG are not gradually increased similar to that

observed when sharing load on the grid and picking up load during surveillance testing. In a

postulated LOOP, the start of large equipment such as an RHR pump motor may result in

higher stress or impact loading to equipment such as the degraded turbochargers inlet check

valve noted in this evaluation. This would just be an additional uncertainty regarding the failure

mechanism and timing. This significance determination process analysis, including assumed

exposure time is thought to capture any of these uncertainties and provide a best estimate risk

evaluation for this issue.