IR 05000277/2010006
ML101180465 | |
Person / Time | |
---|---|
Site: | Peach Bottom |
Issue date: | 04/28/2010 |
From: | Doerflein L Engineering Region 1 Branch 2 |
To: | Pardee C Exelon Generation Co, Exelon Nuclear |
References | |
IR-10-006 | |
Download: ML101180465 (18) | |
Text
UNITED STATES ril 28, 2010
SUBJECT:
PEACH BOTTOM ATOMIC POWER STATION, UNITS 2 AND 3 - NRC EVALUATION OF CHANGES, TESTS, AND EXPERIMENTS AND PERMANENT MODIFICATIONS TEAM INSPECTION REPORT 05000277/2010006 AND 05000278/2010006
Dear Mr. Pardee:
On March 19, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at the Peach Bottom Atomic Power Station. The enclosed inspection report documents the inspection results, which were discussed on March 19, 2010, with Mr. W. Maguire, and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.
In conducting the inspection, the team reviewed selected procedures, calculations and records, observed activities, and interviewed station personnel.
Based on the results of this inspection, no findings of significance were identified.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html(the Public Electronic Reading Room).
Sincerely, c:Yc~~ -f 6o&JOo~
Lawrence T. Doerflein, Chief~! ~
Engineering Branch 2 Division of Reactor Safety Docket Nos.: 50-277; 50-278 License Nos.: DPR-44, DPR-56
Enclosure:
Inspection Report No. 05000277/2010006 and 05000278/2010006 w/Attachment: Supplemental Information
REGION I==
Docket No.: 50-277 and 50-278 License No.: DPR-44 and DPR-56 Report No.: 05000277/2010006 and 05000278/2010006 Licensee: Exelon Generation Company, LLC (Exelon)
Facility: Peach Bottom Atomic Power Station, Units 2 and 3 Location: Delta, Pennsylvania Inspection Period: March 1, 2010 through March 19, 2010 Inspectors: J. Lilliendahl, Reactor Inspector, Division of Reactor Safety (DRS),
Team Leader K. Mangan, Senior Reactor Inspector, DRS M. Orr, Reactor Inspector, DRS S. Rich, Reactor Engineer, NSPDP (in-training)
G. Figueroa, Reactor Systems Engineer, Office of Nuclear Regulatory Research (RES) (observer)
Approved By: Lawrence T. Doerflein, Chief Engineering Branch 2 Division of Reactor Safety Enclosure
SUMMARY OF FINDINGS
IR 05000277/2010006 and 05000278/2010006; 3/1/2010 - 3/19/2010; Peach Bottom Atomic
Power Station, Units 2 and 3; Engineering Specialist Plant Modifications Inspection.
This report covers a two week on-site inspection period of the evaluations of changes, tests, or experiments and permanent plant modifications. The inspection was conducted by three region based engineering inspectors, one inspector in training, and one observer. No findings of significance were identified. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.
NRC-Identified and Self-Revealing Findings
No findings of significance were identified.
Licensee-Identified Violations
None.
ii
REPORT DETAILS
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R17 Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications
.1 Evaluations of Changes, Tests, or Experiments (22 samples)
a. Inspection Scope
The team reviewed six safety evaluations to determine whether the changes to the facility or procedures, as described in the Updated Final Safety Analysis Report (UFSAR), had been reviewed and documented in accordance with 10 CFR 50.59 requirements. In addition, the team evaluated whether Exelon had been required to obtain NRC approval prior to implementing the change. The team interviewed plant staff and reviewed supporting information including calculations, analyses, design change documentation, procedures, the UFSAR, the Technical Specifications (TSs),and plant drawings, to assess the adequacy of the safety evaluations. The team compared the safety evaluations and supporting documents to the guidance and methods provided in Nuclear Energy Institute (NEI) 96-07, "Guidelines for 10 CFR 50.59 Evaluations," as endorsed by NRC Regulatory Guide 1.187, "Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments," to determine the adequacy of the safety evaluations.
The team also reviewed a sample of sixteen 10 CFR 50.59 screenings for which Exelon had concluded that no safety evaluation was required. These reviews were performed to assess whether Exelon's threshold for performing safety evaluations was consistent with 10 CFR 50.59. The sample included design changes, calculations, and procedure changes.
The team reviewed the safety evaluations that Exelon had performed and approved during the time period covered by this inspection (Le., since the last modifications inspection). The screenings and applicability determinations were selected based on the safety significance, risk significance, and complexity of the change to the facility.
In addition, the team compared Exelon's administrative procedures used to control the screening, preparation, review, and approval of safety evaluations to the guidance in NEI 96-07 to determine whether those procedures adequately implemented the requirements of 10 CFR 50.59. The reviewed safety evaluations and screenings are listed in the attachment.
b. Findings
No findings of significance were identified.
.2 Permanent Plant Modifications (10 samples)
.2.1 High Pressure Service Water (HPSW) Orifice Changes
a. Inspection Scope
The team reviewed a modification (Engineering Change Request (ECR) 06-00023) to the HPSW system outlet piping from the Unit 3 '0' residual heat removal (RHR) heat exchanger. The modification installed a multi-hole orifice plate and removed the plugs from another orifice plate in the same line. This change was necessary following the replacement of internal components of the Unit 3 '0' RHR heat exchanger outlet valve, because the newer assembly had a greater resistance coefficient and resultant pressure drop. The team conducted the review to verify that the design bases, licensing bases, and performance capability of the HPSW system had not been degraded by the modification.
The team discussed the modification and design basis with design and system engineers to assess the adequacy of the modification and to verify that the HPSW system had been fully restored to service. Post modification test results were reviewed to ensure the HPSW pressure and flow rate met the acceptance criteria. The 10 CFR 50.59 screening determination associated with this modification was also reviewed as described in section 1R17.1 of this report. Additional documents reviewed are listed in the attachment.
b. Findings
No findings of significance were identified .
.2.2 'E1' Emergency Diesel Generator (EDG) Speed Switch Replacement
a. Inspection Scope
The team reviewed a modification (ECR 07-00284) which replaced the 'E l' EDG engine speed switch. Exelon implemented this modification following erratic behavior of the speed switch during routine surveillance testing. Exelon had previously upgraded the speed switch to a newer model, and did not have any available new spares. The modification re-installed the original model speed switch. The original model speed switch had a successful history of use since plant construction and was determined to meet the criteria of an equivalent change. The team conducted the review to ensure that the design bases, licensing bases, and performance capability of the EDG had not been adversely affected by the modification.
The team reviewed the high and low speed switch setpoints to verify there were no adverse impacts to operating margins and that the speed switch functioned in accordance with the design basis. The team reviewed post maintenance test data to confirm that the replacement speed switch met the acceptance criteria and the EDG was operable. Additionally, the team reviewed the associated work order packages and conducted interviews with design and system engineers regarding the design, installation, and testing of the switches to verify that the modification was adequate.
The team walked down the 'E1' EDG to assess the system configuration. The documents reviewed are listed in the attachment.
b. Findings
No findings of significance were identified .
.2.3 'E1' EDG Tachometer Drive Coupling Shaft/Pin Replacement
a. Inspection Scope
The team reviewed a modification (ECR 09-00360) associated with the replacement of the 'E1' EDG tachometer drive coupling shaft and pins. These components support the EDG's automatic start design function. Exelon implemented this modification following the determination that the tachometer drive coupling shaft and pins had been damaged during engine reassembly. The replacement drive assembly did not include the required shaft and pins, which transfer camshaft rotation through the tachometer drive to the speed switch. This modification consisted of the fabrication of a new shaft and pins identical to the existing components. The team evaluated the change to confirm that the design bases, licensing bases, and performance capability of the EDG had not been inadvertently degraded by the modification.
The team reviewed the plan to fabricate the replacement parts to evaluate the suitability of the replacement material. The team interviewed design engineers with regards to the technical evaluation of material used, material specifications, risk assessment,
.fabrication and acceptable machining tolerances, single point vulnerability review, and acceptance testing. The team reviewed performance test data obtained after the installation of the tachometer drive coupling and the on-site manufactured shaft and pins to verify proper performance of the 'E1' EDG speed switch. The team performed a walkdown of 'E1' EDG to assess the system configuration. The documents reviewed are listed in the attachment.
b. Findings
No findings of significance were identified .
.2.4 Core Spray Pump Technical Specification and In-service Test Acceptance Criteria
a. Inspection Scope
The team reviewed the design change (ECR 08-00074) that revised the acceptance criteria for the core spray pump surveillance tests. Exelon revised calculation ME-0073, Core Spray Pump In-Service Testing Acceptance Criteria, as well as the TS surveillance bases documents. Exelon implemented this design change to ensure pump testing results could be used for both in-service testing (1ST) requirements for differential pressure and TS surveillance requirements which used discharge pressure as an acceptance criterion. The team evaluated the change to ensure that the design bases and licensing bases had not been adversely affected, and performance capability of the core spray system would be properly evaluated against design and licensing requirements.
The team reviewed calculation ME-0073 to determine if the pressure acceptance criterion for each pump had been correctly calculated. Additionally, the team verified the appropriateness of calculation assumptions. The team also reviewed the core spray pump surveillance procedures to confirm that the design change had been incorporated into the procedures and the test configuration ensured design requirements were satisfied. The team assessed past surveillance test data to ensure that any negative trends would be captured by the new criteria. Finally, the team interviewed design and 1ST engineers to discuss the design criteria associated with the change. Documents reviewed are listed in the attachment.
b. Findings
No findings of significance were identified .
.2.5 Modification of MO-3-23-016 Torque Switch
a. Inspection Scope
The team reviewed a modification (ECR 07-00342) that changed the closing logic for the high pressure coolant injection (HPCI) turbine steam line isolation valve, MO-3-23-016.
The valve also has the safety function to close for primary containment isolation. The modification replaced the 2-rotor switch with a 4-rotor switch and bypassed the torque switch stop signal until the valve closed indication was also actuated. Exelon implemented this modification in order to allow the use of the full capability of the valve motor to close the valve rather than be limited by the torque switch setting. The team conducted the review to ensure that the design bases, licensing bases, and performance capabilities of the primary containment isolation system and HPCI system had not been adversely affected by the modification.
The team assessed selected design inputs and attributes to ensure that they were consistent with the design and licensing bases. The team verified that the safety-related component qualification for the new switch was adequate. Additionally, the team confirmed that the new design did not introduce any new failure modes for the valve which could impact the HPCI system design basis accident response. The team also reviewed the post modification test plan and results to ensure appropriate acceptance criteria had been met which demonstrated the adequacy of the new design. Finally, the team interviewed the motor operated valve engineer to discuss the implementation of the modification. The 10 CFR 50.59 screening determination associated with this modification was also reviewed as described in section 1R17.1 of this report.
Documents reviewed are listed in the attachment.
b. Findings
No findings of significance were identified .
.2.6 Implementation of New Technical Specifications for Control Room Envelope
a. Inspection Scope
The team reviewed a modification (ECR 08-00104) to the control room envelope (CRE)habitability program that changed the way operability of the CRE was evaluated. With the change Exelon established a maximum breech size in the envelope as the requirement to ensure its operability. Exelon performed a calculation to determine the size of the maximum opening, based on the capabilities of the main control room emergency ventilation (MCREV) system, as well as the hole size that correlated to the current leakage out of the CRE. Exelon implemented this modification in order to more easily determine the impact of maintenance work on CRE operability. The team conducted the review to ensure that the design bases, licensing bases, and performance capabilities of the CRE and MCREV system had not been adversely affected by the modification.
The team reviewed calculation PM-1081, Calculation of ~aximum CRE Breach, to determine that the maximum opening size had been correctly calculated and that assumptions used in the calculation were appropriate. The team also reviewed completed copies of procedure GP-30, Control Room Envelope Boundary Integrity, to verify that the opening size limits were being maintained. The team interviewed the design engineer to discuss the design criteria associated with the change, and walked down the CRE with the program engineer to ensure that conditions in the field aligned with the calculation assumptions. Documents reviewed are listed in the attachment.
b. Findings
No findings of significance were identified .
.2.7 Unit 3 Cycle 16 Core Reload Analysis
a. Inspection Scope
The team reviewed the analysis performed by Exelon for the design of the Unit 3 cycle 16 core reload (ECR 07-00158). The analysis was performed to ensure that various core parameters and thermal limits would not be exceeded throughout the life of the core. The team conducted the review to ensure that the design bases and licensing bases for the fuel had not been adversely affected by the modification. The team reviewed the analysis to determine what codes were used in the core design and compared those codes to the codes approved by the NRC as listed in the UFSAR. The team also reviewed any changes made by the fuel vendor to the approved codes to ensure that changes made to the approved methodologies resulted in conservative results. Additionally, the team reviewed the results from start-up physics testing to verify that appropriate acceptance criteria had been applied and the testing results were within the acceptance criteria. Documents reviewed are listed in the attachment.
b. Findings
No findings of significance were identified .
.2.8 Modification to Provide Continuous Prelube for 'E1' EDG
a. Inspection Scope
The team reviewed a modification (ECR 05-00255) which provided continuous prelube of the 'E1' EDG lower crankshaft line. Exelon implemented the modification to keep the system piping, filters, strainers, and heat exchangers filled so that lube oil will be quickly provided to the bearings in the event of an emergency start. The modification included replacing the existing lube oil heater with a higher kilowatt rated heater, and adding a thermostatically controlled valve that allows oil to flow to the engine lower crankshaft line only after it has reached a sufficient temperature. The team conducted the review to ensure that the design bases, licensing bases, and performance capability of the EDG had not been adversely affected by the modification.
The team assessed selected design inputs and attributes to ensure that they were consistent with the design and licensing bases. The team interviewed the responsible design and system engineers to understand the implementation of the modification and subsequent system performance. The team reviewed the electrical loading calculations and breaker coordination calculations to assess the adequacy of the design with respect to the additional heater load. Additionally, the team evaluated if the design introduced any new failure modes for the lube oil system which could impact EDG design basis accident response. The team also reviewed the post modification test plan and results to ensure appropriate acceptance criteria had been met and the tests demonstrated the adequacy of the new design. The 10 CFR 50.59 screening determination associated with this modification was also reviewed as described in section 1R17.1 of this report.
Documents reviewed are listed in the attachment.
b. Findings
No findings of significance were identified.
.2.9 Modification to Replace Electro-Mechanical Trip Devices with Solid State Trip Devices
a. Inspection Scope
The team reviewed a modification (ECR 07-00001) which replaced the electro-mechanical trip devices in safety related 480V breakers with solid state trip devices.
Exelon implemented the modification because the electro-mechanical devices were obsolete. The modification included replacing the trip devices, setting the new trip device setpoints, and updating the breaker coordination calculation. The breaker coordination calculation was updated to verify that the new device trip characteristics would provide adequate coordination. The team conducted the review to ensure that the design bases, licensing bases, and performance capability of the safety related 480V system had not been adversely affected by the modification.
The team assessed selected design inputs and attributes to ensure that they were consistent with the design and licensing bases. The team interviewed the responsible design engineer to understand the implementation of the modification and subsequent system performance. The team reviewed the original and revised versions of PE-0193, Coordination Study for 480VAC Load Centers and Motor Control Centers (MCCs), to assess the adequacy of the design with respect to the new trip device characteristics and the new trip settings. The team also reviewed the post modification test plan and results to ensure that the actual trip settings were in accordance with the design trip settings. The associated equivalency change evaluation was also reviewed.
Documents reviewed are listed in the attachment.
b. Findings
No findings of significance were identified .
.2.10 Modification to Retire 'E3' EDG Auxiliary Pumps and Associated Breaker Change
a. Inspection Scope
The team reviewed a modification (ECR 08-00017) that retired the 'E3' EDG jacket coolant, air coolant, and lube oil motor driven backup auxiliary pumps. Exelon implemented the modification because the aforementioned pumps required excessive maintenance, introduced leak paths, increased the failure modes, and did not appreciably increase the reliability of the EDGs. Exelon had previously completed this modification for the other EDGs. The modification included isolating and removing the pumps (blind flanges, etc.), removing the pump power and controls, and replacing the EDG MCC instantaneous magnetic molded case circuit breakers (MCCBs) with thermal magnetic MCCBs. The team conducted the review to ensure that the design bases, licensing bases, and performance capability of the EDG had not been adversely affected by the modification.
.
The team assessed selected design inputs and attributes to ensure that they were consistent with the design and licensing bases. The team interviewed the responsible design and system engineers to understand the implementation of the modification and subsequent system performance. The team reviewed the breaker coordination calculations to assess the adequacy of the design with respect to the change in circuit breaker design. Additionally, the team confirmed that the design did not introduce any new failure modes for the lube oil system, jacket water system, or air cooling system which could impact EDG design basis accident response. The team also reviewed the post modification test plan and results to ensure appropriate acceptance criteria had been met and the tests demonstrated the adequacy of the new design. Finally, the team walked down the 'E3' EDG to verify that the retired equipment was fully isolated from the EDG. The 10 CFR 50.59 screening determination associated with this modification was also reviewed as described in section 1R 17.1 of this report.
Documents reviewed are listed in the attachment.
b. Findings
No findings of significance were identified.
OTHER ACTIVITIES
40A2 Identification and Resolution of Problems (IP 71152)
a. Inspection Scope
The team reviewed a sample of Issue Reports (IRs) associated with 10 CFR 50.59 and plant modification issues to determine whether Exelon was appropriately identifying, characterizing, and correcting problems associated with these areas, and whether the planned or completed corrective actions were appropriate. In addition, the team reviewed IRs written on issues identified during the inspection to verify adequate problem identification and incorporation of the problem into the corrective action system.
The IRs reviewed are listed in the attachment.
b. Findings
No findings of significance were identified.
40A6 Meetings. including Exit The team presented the inspection results to Mr. W. Maguire, Site Vice President, and other members of Exelon's staff at an exit meeting on March 19,2010. The team returned the proprietary information reviewed during the inspection to the licensee and verified that this report does not contain proprietary information.
ATTACHMENT
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Exelon' Personnel
- W. Maguire, Site Vice President
- R. Smith, Licensing
- J. Chizever, Manager, Mechanical Design Engineering
- K. Cutler, Design Engineer
LIST OF ITEMS
OPENED, CLOSED AND DISCUSSED
None.