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Category:CORRESPONDENCE-LETTERS
MONTHYEARSVP-99-181, Forwards Biennial Update to Quad Cities Ufsar,Iaw 10CFR50.71(e).Update Includes Changes to Facility & Procedures & Are Current Through 9906301999-10-20020 October 1999 Forwards Biennial Update to Quad Cities Ufsar,Iaw 10CFR50.71(e).Update Includes Changes to Facility & Procedures & Are Current Through 990630 ML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20217K7011999-10-13013 October 1999 Provides Response to Questions Related to Request for License Amend,Per 10CFR50.90, Credit for Containment Overpressure. Supporting Calculations Encl 05000254/LER-1999-004, Forwards LER 99-004-00,IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Is Committed to Listed Action1999-10-12012 October 1999 Forwards LER 99-004-00,IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Is Committed to Listed Action ML20217F6321999-10-0707 October 1999 Forwards Insp Repts 50-254/99-01 & 50-265/99-01 on 990721- 0908.No Violations 05000254/LER-1999-003, Forwards LER 99-003-00 IAW 10CFR73(a)(2)(v)(A).Commitment Made by Util,Listed.Any Other Actions Described in LER Represent Intended or Planned Actions by Licensee1999-10-0707 October 1999 Forwards LER 99-003-00 IAW 10CFR73(a)(2)(v)(A).Commitment Made by Util,Listed.Any Other Actions Described in LER Represent Intended or Planned Actions by Licensee ML20212K9421999-10-0505 October 1999 Informs That NRC Accepts 990513 Inservice Inspection Relief Request CR-31 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr SVP-99-189, Confirms Completion of Actions Identified During Review of NRC Safety Evaluation of Boiling Water Reactor Owners Group Rept, Utility Resolution Guidance of ECCS Suction Strainer Blockage1999-09-22022 September 1999 Confirms Completion of Actions Identified During Review of NRC Safety Evaluation of Boiling Water Reactor Owners Group Rept, Utility Resolution Guidance of ECCS Suction Strainer Blockage ML20212J0451999-09-21021 September 1999 Forwards Safety Evaluation of Licensee USI A-46 Program at Quad Cities Nuclear Power Station,Units 1 & 2,established in Response to GL 87-02 Through 10CFR50.54(f) Ltr ML20212D8231999-09-20020 September 1999 Informs That Effectieve 991101,NRC Region III Will Be Conducting Safety System Design & Performance Capability Pilot Insp at Quad Cities Nuclear Power Station.Insp Will Be Performed IAW NRC Pilot Insp Procedure 71111-21 ML20212C6961999-09-15015 September 1999 Forwards Insp Repts 50-254/99-17 & 50-265/99-17 on 990823- 0827.No Violations Noted SVP-99-190, Clarifies Statement Contained in NRC Insp Repts 50-254/99-12 & 50-265/99-12,dtd 990813,paragraph 4OA1.3B, Observation & Findings, Re Sys Mod to DG Air Start Sys1999-09-13013 September 1999 Clarifies Statement Contained in NRC Insp Repts 50-254/99-12 & 50-265/99-12,dtd 990813,paragraph 4OA1.3B, Observation & Findings, Re Sys Mod to DG Air Start Sys ML20211Q7961999-09-0909 September 1999 Forwards Correction to Administrative Error on Page 8 of NRC Insp Repts 50-254/99-16 & 50-265/99-16,transmitted by Ltr, ML20217H5661999-09-0909 September 1999 Discusses 990907 Pilot Plan Mgt Meeting Re Results to-date of Pilot Implementation of NRC Revised Reactor Oversight Process at Prairie Island & Quad Cities.Agenda & Handouts Provided by Utils Encl ML20211Q6511999-09-0808 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Quad Cities Operator License Applicants During Wk of 000327.Validation of Exam Will Occur at Station During Wk of 000306 ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) ML20211F8251999-08-25025 August 1999 Forwards Insp Repts 50-254/99-15 & 50-265/99-15 on 990816-20.No Violations Noted.Insp Evaluated Effectiveness of Maint Rule Program & Review Periodic Evaluation Specifically Required for 10CFR50.65 ML20211B8691999-08-20020 August 1999 Forwards Insp Repts 50-254/99-10,50-265/99-10,50-454/99-09, 50-455/99-09,50-456/99-10 & 50-457/99-10 on 990628-0721. Action Plans Developed to Address Configuration Control Weaknesses Not Totally Effective as Listed ML20211D1491999-08-19019 August 1999 Forwards Insp Repts 50-254/99-16 & 50-265/99-16 on 990719-22.Staff Identified Major Discrepancy Re Accuracy of Data Submitted to NRC for Protected Area Security Equipment Performance ML20211C7601999-08-19019 August 1999 Confirms NRC Intent to Meet with NSP & Ceco on 990807 in Lisle,Il to Discuss with Region III Pilot Plants,Any Observations,Feedback,Lessons Learned & Recommendations Relative to Implementation of Pilot Program ML20210R7451999-08-13013 August 1999 Forwards Insp Repts 50-254/99-11 & 50-265/99-11 on 990601-0720.NRC Identified Several Issues Which Were Categorized as Being of Low Risk Significance.Two Issues Involved NCVs of Regulatory Requirements SVP-99-147, Notifies of Change to Bases of TS to Licenses DPR-29 & DPR- DPR-30.Change to TS Section 3/4.9 Provides Clarity & Consistency with Sys Design Description in Ufsar,Sections 8.3.2.1 & 8.3.2.2.TS Bases Page,Encl1999-08-13013 August 1999 Notifies of Change to Bases of TS to Licenses DPR-29 & DPR- DPR-30.Change to TS Section 3/4.9 Provides Clarity & Consistency with Sys Design Description in Ufsar,Sections 8.3.2.1 & 8.3.2.2.TS Bases Page,Encl SVP-99-170, Forwards Relief Requests CR-25,CR-26,CR-27,CR-28,PR-11, PR-12 & PR-13,on Basis That Compliance with Specified Requirements Would Result in Hardship or Unusual Difficulty Without Compensating Increase in Level of Quality & Safety1999-08-13013 August 1999 Forwards Relief Requests CR-25,CR-26,CR-27,CR-28,PR-11, PR-12 & PR-13,on Basis That Compliance with Specified Requirements Would Result in Hardship or Unusual Difficulty Without Compensating Increase in Level of Quality & Safety ML20210T9941999-08-13013 August 1999 Forwards Insp Repts 50-254/99-12 & 50-265/99-12 on 990628-0716.Violations Noted SVP-99-154, Notifies NRC That M Price,License SOP-31389,is No Longer Required to Maintain Operator License.Price Was Removed from Licensed Duty on 990729 & Comm Ed Requests License Be Terminated1999-08-13013 August 1999 Notifies NRC That M Price,License SOP-31389,is No Longer Required to Maintain Operator License.Price Was Removed from Licensed Duty on 990729 & Comm Ed Requests License Be Terminated ML20210R9541999-08-10010 August 1999 Informs That During 990804 Telcon Between J Bartlet & M Bielby,Arrangements Were Made for NRC to Insp License Operator Requalification Program at Plant.Insp Planned for Wks of 991018 & 25 ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210M5461999-08-0606 August 1999 Discusses 990804 Telcon Between J Bartlet & M Bielby,Where Arrangements Were Made for NRC to Inspect Licensed Operator Requalification Program at Plant.Insp Planned for Wks of 991018 & 25 ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed ML20210L8371999-08-0202 August 1999 Forwards SE Accepting Licensee 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety Related Motor-Operated Valves ML20210M4691999-07-30030 July 1999 Forwards Insp Repts 50-254/99-14 & 50-265/99-14 on 990713-15.One NCV Was Identified & Discussed in Encl Insp ML20210H4661999-07-29029 July 1999 Forwards Insp Repts 50-254/99-13 & 50-265/99-13 on 990628-0702.No Violations Noted.Insp Consisted of Selective Examination of Procedures & Representative Records, Observations of Activities & Interviews with Personnel 05000254/LER-1999-002, Forwards LER 99-002-01,IAW 10CFR50.73(a)(2)(iv).Rev Includes Cause Codes & Energy Industry Identification Sys Identifiers Which Were Erroneously Omitted in Original Ler.Commitments Listed1999-07-29029 July 1999 Forwards LER 99-002-01,IAW 10CFR50.73(a)(2)(iv).Rev Includes Cause Codes & Energy Industry Identification Sys Identifiers Which Were Erroneously Omitted in Original Ler.Commitments Listed SVP-99-151, Responds to NRC 990701 Telcon RAI Re Licensee Amend Request Re Use of Containment Overpressure to Support NPSH Available for ECCS at Quad Cities Nuclear Power Station,Units 1 & 21999-07-23023 July 1999 Responds to NRC 990701 Telcon RAI Re Licensee Amend Request Re Use of Containment Overpressure to Support NPSH Available for ECCS at Quad Cities Nuclear Power Station,Units 1 & 2 SVP-99-150, Forwards Responses to 990520 RAI Re Annual 10CFR50.46 Rept1999-07-23023 July 1999 Forwards Responses to 990520 RAI Re Annual 10CFR50.46 Rept SVP-99-146, Informs of Termination of License SOP-31132-1,for G Green, as Required by 10CFR50.74(b).Individual Was Removed from License Duty on 9906251999-07-21021 July 1999 Informs of Termination of License SOP-31132-1,for G Green, as Required by 10CFR50.74(b).Individual Was Removed from License Duty on 990625 ML20210B7071999-07-16016 July 1999 Responds to Requesting Review & Approval of Three Proposed Changes to Ceco QA TR,CE-1A Per 10CFR50.54(a)(3) & 10CFR50.4(b)(7) ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes SVP-99-139, Forwards Revised Action 2 & Associated TS Bases Changes, Describing Specific Alternate Method for Determining Drywell Floor Drain Sump Leakage1999-06-30030 June 1999 Forwards Revised Action 2 & Associated TS Bases Changes, Describing Specific Alternate Method for Determining Drywell Floor Drain Sump Leakage ML20209B2081999-06-29029 June 1999 Discusses Closure of Response to RAI Re GL 92-01,Rev 1,Suppl 1, Reactor Vessel Structural Integrity. Rvid,Version 2 Issued as Result of Review of Responses.Info Should Be Reviewed & Comments Submitted by 990901 05000265/LER-1999-002, Forwards LER 99-002-00 for Quad Cities Nuclear Power Station IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Commits to One Listed Action1999-06-25025 June 1999 Forwards LER 99-002-00 for Quad Cities Nuclear Power Station IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Commits to One Listed Action SVP-99-122, Forwards Regulatory Commitment Change Summary Rept, Containing Summary Info from 980601 Through 9906011999-06-25025 June 1999 Forwards Regulatory Commitment Change Summary Rept, Containing Summary Info from 980601 Through 990601 SVP-99-066, Informs That J Reed,License SOP-31034-1,was Removed from License Duty in 990618.Termination of License Is Requested1999-06-25025 June 1999 Informs That J Reed,License SOP-31034-1,was Removed from License Duty in 990618.Termination of License Is Requested SVP-99-103, Informs NRC of Results of Subject Evaluation as Committed to in .Evaluation Consisted of Analytically Demonstrating That Cfu Factor for Rv Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period1999-06-25025 June 1999 Informs NRC of Results of Subject Evaluation as Committed to in .Evaluation Consisted of Analytically Demonstrating That Cfu Factor for Rv Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period ML20196F7921999-06-24024 June 1999 Forwards Meeting Summary,Nrc Meeting Handout & Licensee Handout from 990608 Meeting ML20196E7131999-06-23023 June 1999 Forwards Insp Repts 50-254/99-09 & 50-265/99-09 on 990421-0531.One Violation of NRC Requirements Occurred & Being Treated as non-cited Violation,Consistent with App C of Enforcement Policy ML20196E4821999-06-21021 June 1999 Discusses 990617 Meeting by Region III Senior Reactor Analysts (SRA) in Cordova,Il to Meet with PRA Staff to Discuss Initiatives in Risk Area & to Establish Dialog Between SRAs & PRA Staff 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARSVP-99-181, Forwards Biennial Update to Quad Cities Ufsar,Iaw 10CFR50.71(e).Update Includes Changes to Facility & Procedures & Are Current Through 9906301999-10-20020 October 1999 Forwards Biennial Update to Quad Cities Ufsar,Iaw 10CFR50.71(e).Update Includes Changes to Facility & Procedures & Are Current Through 990630 ML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20217K7011999-10-13013 October 1999 Provides Response to Questions Related to Request for License Amend,Per 10CFR50.90, Credit for Containment Overpressure. Supporting Calculations Encl 05000254/LER-1999-004, Forwards LER 99-004-00,IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Is Committed to Listed Action1999-10-12012 October 1999 Forwards LER 99-004-00,IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Is Committed to Listed Action 05000254/LER-1999-003, Forwards LER 99-003-00 IAW 10CFR73(a)(2)(v)(A).Commitment Made by Util,Listed.Any Other Actions Described in LER Represent Intended or Planned Actions by Licensee1999-10-0707 October 1999 Forwards LER 99-003-00 IAW 10CFR73(a)(2)(v)(A).Commitment Made by Util,Listed.Any Other Actions Described in LER Represent Intended or Planned Actions by Licensee ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr SVP-99-189, Confirms Completion of Actions Identified During Review of NRC Safety Evaluation of Boiling Water Reactor Owners Group Rept, Utility Resolution Guidance of ECCS Suction Strainer Blockage1999-09-22022 September 1999 Confirms Completion of Actions Identified During Review of NRC Safety Evaluation of Boiling Water Reactor Owners Group Rept, Utility Resolution Guidance of ECCS Suction Strainer Blockage SVP-99-190, Clarifies Statement Contained in NRC Insp Repts 50-254/99-12 & 50-265/99-12,dtd 990813,paragraph 4OA1.3B, Observation & Findings, Re Sys Mod to DG Air Start Sys1999-09-13013 September 1999 Clarifies Statement Contained in NRC Insp Repts 50-254/99-12 & 50-265/99-12,dtd 990813,paragraph 4OA1.3B, Observation & Findings, Re Sys Mod to DG Air Start Sys ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) SVP-99-154, Notifies NRC That M Price,License SOP-31389,is No Longer Required to Maintain Operator License.Price Was Removed from Licensed Duty on 990729 & Comm Ed Requests License Be Terminated1999-08-13013 August 1999 Notifies NRC That M Price,License SOP-31389,is No Longer Required to Maintain Operator License.Price Was Removed from Licensed Duty on 990729 & Comm Ed Requests License Be Terminated SVP-99-170, Forwards Relief Requests CR-25,CR-26,CR-27,CR-28,PR-11, PR-12 & PR-13,on Basis That Compliance with Specified Requirements Would Result in Hardship or Unusual Difficulty Without Compensating Increase in Level of Quality & Safety1999-08-13013 August 1999 Forwards Relief Requests CR-25,CR-26,CR-27,CR-28,PR-11, PR-12 & PR-13,on Basis That Compliance with Specified Requirements Would Result in Hardship or Unusual Difficulty Without Compensating Increase in Level of Quality & Safety SVP-99-147, Notifies of Change to Bases of TS to Licenses DPR-29 & DPR- DPR-30.Change to TS Section 3/4.9 Provides Clarity & Consistency with Sys Design Description in Ufsar,Sections 8.3.2.1 & 8.3.2.2.TS Bases Page,Encl1999-08-13013 August 1999 Notifies of Change to Bases of TS to Licenses DPR-29 & DPR- DPR-30.Change to TS Section 3/4.9 Provides Clarity & Consistency with Sys Design Description in Ufsar,Sections 8.3.2.1 & 8.3.2.2.TS Bases Page,Encl ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed 05000254/LER-1999-002, Forwards LER 99-002-01,IAW 10CFR50.73(a)(2)(iv).Rev Includes Cause Codes & Energy Industry Identification Sys Identifiers Which Were Erroneously Omitted in Original Ler.Commitments Listed1999-07-29029 July 1999 Forwards LER 99-002-01,IAW 10CFR50.73(a)(2)(iv).Rev Includes Cause Codes & Energy Industry Identification Sys Identifiers Which Were Erroneously Omitted in Original Ler.Commitments Listed SVP-99-150, Forwards Responses to 990520 RAI Re Annual 10CFR50.46 Rept1999-07-23023 July 1999 Forwards Responses to 990520 RAI Re Annual 10CFR50.46 Rept SVP-99-151, Responds to NRC 990701 Telcon RAI Re Licensee Amend Request Re Use of Containment Overpressure to Support NPSH Available for ECCS at Quad Cities Nuclear Power Station,Units 1 & 21999-07-23023 July 1999 Responds to NRC 990701 Telcon RAI Re Licensee Amend Request Re Use of Containment Overpressure to Support NPSH Available for ECCS at Quad Cities Nuclear Power Station,Units 1 & 2 SVP-99-146, Informs of Termination of License SOP-31132-1,for G Green, as Required by 10CFR50.74(b).Individual Was Removed from License Duty on 9906251999-07-21021 July 1999 Informs of Termination of License SOP-31132-1,for G Green, as Required by 10CFR50.74(b).Individual Was Removed from License Duty on 990625 ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes SVP-99-139, Forwards Revised Action 2 & Associated TS Bases Changes, Describing Specific Alternate Method for Determining Drywell Floor Drain Sump Leakage1999-06-30030 June 1999 Forwards Revised Action 2 & Associated TS Bases Changes, Describing Specific Alternate Method for Determining Drywell Floor Drain Sump Leakage SVP-99-103, Informs NRC of Results of Subject Evaluation as Committed to in .Evaluation Consisted of Analytically Demonstrating That Cfu Factor for Rv Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period1999-06-25025 June 1999 Informs NRC of Results of Subject Evaluation as Committed to in .Evaluation Consisted of Analytically Demonstrating That Cfu Factor for Rv Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period SVP-99-122, Forwards Regulatory Commitment Change Summary Rept, Containing Summary Info from 980601 Through 9906011999-06-25025 June 1999 Forwards Regulatory Commitment Change Summary Rept, Containing Summary Info from 980601 Through 990601 05000265/LER-1999-002, Forwards LER 99-002-00 for Quad Cities Nuclear Power Station IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Commits to One Listed Action1999-06-25025 June 1999 Forwards LER 99-002-00 for Quad Cities Nuclear Power Station IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Commits to One Listed Action SVP-99-066, Informs That J Reed,License SOP-31034-1,was Removed from License Duty in 990618.Termination of License Is Requested1999-06-25025 June 1999 Informs That J Reed,License SOP-31034-1,was Removed from License Duty in 990618.Termination of License Is Requested SVP-99-125, Forwards Technical Info Re ECCS Suction Strainers at Quad Cities Nuclear Power Station Units 1 & 2,to Support Review of 990129 Lar.Rev 0 to TR-VQ1500-02, Clean ECCS Suction Strainer Head Loss Test Rept, Encl1999-06-15015 June 1999 Forwards Technical Info Re ECCS Suction Strainers at Quad Cities Nuclear Power Station Units 1 & 2,to Support Review of 990129 Lar.Rev 0 to TR-VQ1500-02, Clean ECCS Suction Strainer Head Loss Test Rept, Encl ML20195E3491999-06-0707 June 1999 Withdraws Util Requesting License Change for Plant Security Plan Rev.Licensee Will re-evaluate Situation & May Request Approval of Change in Future ML20207G1451999-06-0707 June 1999 Forwards Rev 45 to Comed Quad Cities Nuclear Power Station Security Plan.Rev Includes Changes Listed.Security Plan Is Withheld from Public Disclosure Per 10CFR73.21 ML20195D6351999-06-0404 June 1999 Notifies NRC of Actions That Has Been Taken in Accordance with 10CFR26, Fitness for Duty Programs SVP-99-105, Informs NRC of Rev to Schedule for Completing Setpoint/ Uncertainty Calculations & Procedure Changes,Originally Planned for Completion on 9905291999-05-20020 May 1999 Informs NRC of Rev to Schedule for Completing Setpoint/ Uncertainty Calculations & Procedure Changes,Originally Planned for Completion on 990529 ML20195B2301999-05-19019 May 1999 Requests Approval of Proposed Changes to QA Topical Rept CE-1-A,rev 66a.Attachment a Describes Changes,Reason for Change & Basis for Concluding That Revised QAP Incorporating Proposed Changes Continues to Satisfy 10CFR50AppB SVP-99-111, Informs NRC of Current Status of Actions on Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions1999-05-17017 May 1999 Informs NRC of Current Status of Actions on Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions SVP-99-098, Fulfills Thirty Day & Annual Reporting Requirements of 10CFR50.46 for Plant.Eccs Evaluation Change Rept Transmitted in Entirety,Fulfilling Thirty Day & Annual Reporting Requirements Specified in 10CFR50.46(a)(3)(i)1999-05-17017 May 1999 Fulfills Thirty Day & Annual Reporting Requirements of 10CFR50.46 for Plant.Eccs Evaluation Change Rept Transmitted in Entirety,Fulfilling Thirty Day & Annual Reporting Requirements Specified in 10CFR50.46(a)(3)(i) SVP-99-099, Requests Relief from Requirements of 10CFR50.55a(g) Re Submittal of Relief Requests for Those Welds for Which Examinations of Greater than 90% of Weld Vol Was Not Acheived During 2nd ISI Program Interval1999-05-13013 May 1999 Requests Relief from Requirements of 10CFR50.55a(g) Re Submittal of Relief Requests for Those Welds for Which Examinations of Greater than 90% of Weld Vol Was Not Acheived During 2nd ISI Program Interval SVP-99-096, Provides Suppl Response to Violations Noted in Insp Repts 50-254/98-20 & 50-265/98-23.Corrective Actions:Listed Multidiscipline Team Will Perform self-assessment IAW Station Program for self-assessments in May 19991999-05-12012 May 1999 Provides Suppl Response to Violations Noted in Insp Repts 50-254/98-20 & 50-265/98-23.Corrective Actions:Listed Multidiscipline Team Will Perform self-assessment IAW Station Program for self-assessments in May 1999 05000254/LER-1999-001, Forwards LER 99-001-00 for Quad Cities Nuclear Power Station.Licensee Shall Rept Any Operation or Condition Prohibited by Plant Tech Specs.Util Committing to Listed Actions1999-05-12012 May 1999 Forwards LER 99-001-00 for Quad Cities Nuclear Power Station.Licensee Shall Rept Any Operation or Condition Prohibited by Plant Tech Specs.Util Committing to Listed Actions ML20206F5381999-04-30030 April 1999 Forwards Magnetic Tape Containing Annual Dose Repts for 1998 for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR20.2206(c).Without Magnetic Tape SVP-99-108, Forwards Quad Cities 1998 Radiological Environ Operating Rept, IAW Plant TS 6.9.A.3.Rept Contains Results of Radiological Environ & Meteorological Monitoring Programs. Radioactive Effluent Release Rept Was Submitted 9903301999-04-30030 April 1999 Forwards Quad Cities 1998 Radiological Environ Operating Rept, IAW Plant TS 6.9.A.3.Rept Contains Results of Radiological Environ & Meteorological Monitoring Programs. Radioactive Effluent Release Rept Was Submitted 990330 SVP-99-036, Forwards Reg Guide 1.16 Rept Number of Personnel-Rem by Work & Job Function for 1998. Associated Collective Deep Dose Equivalent Reported According to Work & Job Functions1999-04-29029 April 1999 Forwards Reg Guide 1.16 Rept Number of Personnel-Rem by Work & Job Function for 1998. Associated Collective Deep Dose Equivalent Reported According to Work & Job Functions SVP-99-088, Informs That Util Is Withdrawing IST Relief Rquests RV-02B & RV-03B1999-04-29029 April 1999 Informs That Util Is Withdrawing IST Relief Rquests RV-02B & RV-03B ML20205T1141999-04-22022 April 1999 Provides Comments from Technical Review of Draft Info Notice Re Unanticipated Reactor Water Draindown at Quad Cities Nuclear Power Station,Unit 2,ANO,Unit 2 & JAFNPP ML20206B2471999-04-20020 April 1999 Informs That SE Kuczynski Has Been Transferred to Position No Longer Requiring SRO License.Cancel License SOP-31030-1, Effective 990412 SVP-99-065, Requests That License SOP-31516,for Jf Graham,Be Terminated, Per 10CFR50.74(b).Individual Was Removed from License Duty on 990319 & No Longer Requires Operator License1999-04-14014 April 1999 Requests That License SOP-31516,for Jf Graham,Be Terminated, Per 10CFR50.74(b).Individual Was Removed from License Duty on 990319 & No Longer Requires Operator License SVP-99-058, Submits Plant Specific ECCS Evaluation Changes,Per Annual Reporting Requirements of 10CFR50.46.Attachments Include Current Assessment Data Re PCT Info Limiting LOCA Evaluations1999-04-14014 April 1999 Submits Plant Specific ECCS Evaluation Changes,Per Annual Reporting Requirements of 10CFR50.46.Attachments Include Current Assessment Data Re PCT Info Limiting LOCA Evaluations SVP-99-063, Responds to NRC Re Violations Noted in Insp Repts 50-254/98-21 & 50-265/98-21.Corrective Actions:Revised Site ISI Procedure Qcap 0410-06, ISI Plan Implementation for Third Ten Year Insp Interval1999-04-0909 April 1999 Responds to NRC Re Violations Noted in Insp Repts 50-254/98-21 & 50-265/98-21.Corrective Actions:Revised Site ISI Procedure Qcap 0410-06, ISI Plan Implementation for Third Ten Year Insp Interval JAFP-99-0129, Submits Comments on Technical Review of Draft Info Notice Describing Unanticipated Reactor Water Draindown at Quad Cities Unit 2,ANO & FitzPatrick1999-04-0909 April 1999 Submits Comments on Technical Review of Draft Info Notice Describing Unanticipated Reactor Water Draindown at Quad Cities Unit 2,ANO & FitzPatrick SVP-99-057, Notifies of Change to Bases for TSs Section 3/4.5, ECCS, Re1999-04-0505 April 1999 Notifies of Change to Bases for TSs Section 3/4.5, ECCS, Re ML20205K5841999-03-31031 March 1999 Submits Rept on Status of Decommissioning Funding for Reactors Owned by Comm Ed.Attachment 1 Contains Amount of Decommissioning Funds Estimated to Be Required Pursuant to 10CFR50.75(b) & (C) SVP-99-062, Informs NRC of Rev to Schedule for Analytically Demonstrating That Cumulative Usage Factor for Reactor Vessel Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period1999-03-31031 March 1999 Informs NRC of Rev to Schedule for Analytically Demonstrating That Cumulative Usage Factor for Reactor Vessel Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period 1999-09-30
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G)mmonwealth I Alimn Onnp.my
. Quad Citio Generating Station 2271o 2W>th Avenue North Cordma. !!.612 AP17 to Tel .w>6n224 -
SVP-98-095 March 13,1998
- U. S. Nuclear Regulatory Commission
. Washington, D. C. 20555 Attention: Document Control Desk
Subject:
- Quad Cities Station Units I and 2 NRC Docket Numbers 50-254 and 50-265 NRC Inspection Report Numbers 50-254/97022 and 50-265/97022
Reference:
J. A. Grobe to 0. D. Kingsley letter dated February 13,1998 Enclosed is Commomvealth Edison's (Comed's) responses to the Notices of Violation (NOV) transmitted with the referenced letter. The report contained four Level IV violations:
Violation 97-022-01 cited a failure to provide adequate procedural instruction for operators to perform QCOP 2300-08, "HPCI Local Manual Operations", Revision 10.
Violation 97-022-03 cited a failure to address the additional alternating current (AC) inboard isolation valve closure time during a loss of offsite power event.
Violation 97-022-04a and 04b cited a failure to follow station procedure requirements for 50.59 screenings.
Violation 97-022-06 cited a failure to follow station procedure requirements for 50.59 report submittals.
This letter contains the following commitments: [
/
For Violation 97-022-01:
No new commitments were made for this violation. N 1
9003240059 980313 PDR ADOCK 05000254:
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' A t)nicom C6mp.my
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USNRC SVP-98-095 ' 2 March 13,1998
. For Violation 97-022-03:
- 1. The 10CFR50.59 associated with modifications will be revised.
(NTS # 254-100-97-02203.01, due April 30,1998.)
2i Training will be provided in Modifications and Lessons Learned that will address logic changes associated with design changes. This activity will be tracked by NTS # 254-100-97-02203.02 and will be complete by July 1,1998.
- 3. Conduct 50.59 Workshop training for the defined complement of preparers and reviewers. This will be accomplished by August 30,1998.
(NTS # 254-100-97-02203.03, due August 30,1998.)
For Violation 97-022-04a and 04b:
- 1. See corrective action for violation 50-254 and 50-265/97022-03.
(NTS # 254-100-97-02203.03, due August 30,1998.)
For Violation 97-022-06:
- 1. Applicable SEs, not previously submitted, will be submitted to the NRC by March 31,1998. (NTS item 254-180-97-SCAQ0002401, due March 31,1998.)
If there are any questions or conunents concerning this letter, please refer them to Mr. Charles Peterson, Regulatory Affairs Manager, at (309) 654-2241, ext. 3609.
Res >ctfully, i
j8 Da id A. Sager b h(h /4/
Site Vice President Quad Cities Station Attachment A, " Responses to Notices of Violation" cc: A. B. Beach, Regional Administrator, Region 111 R. M. Pulsifer, Project Manager, NRR C. G. Miller, Senior Resident Inspector, Quad Cities W. D. Leech, MidAmerican Energy Company
- D. C. Tubbs, MidAmerican Energy Company F. A. Spangenberg, Regulatory Affairs Manager, Dresden INPO Records Center Office of Nuclear Facility Safety, IDNS DCD License (both electronic and hard copies)
M. E. Wagner, Licensing, Comed SVP Letter File
NITACIIMENT A RESPONSE TO NOTICE OF VIOLATION SVP-98-095
. (Page 1 of 7)
NOTICE OF VIOLATION (50-254(265)/97022-01) 10 CFR 50, Appendix B, Criterion V, " Instructions, Procedures and Drawings," requires that activities affecting quality shall be prescribed by documented procedures of a type appropriate to the circumstances and shall be accomplished in accordance with these procedures.
A. Contrary to the above, as of October 27,1997, local manual operation of the liigh Pressure Coolant Injection (HPCI) system, an activity affecting quality, could not be perfonned in accordance with its written procedure QCOP 2300-08, "HPCI Local Manual Operations," Revision 10. Specifically, the procedure steps to rapidly open Unit I and Unit 2 IIPCI steam isolation valves MO 1(2)-2301-4 could not be perfonned because the steps instructed operators to place jumpers between tenninals that did not exist.
This is a Severity Level IV violation (Supplement 1). (50-254/97022-01; 50-265/97022-01)
REASON FOR TIIE VIOLATION:
Comed accepts this violation.
The reason for the incorrect panel designation was human error during procedure development.
On December i 1,1992, QCOP 2300-8, Revision 3, was approved. The panel designations were transposed during the development of Revision 3. A procedure verification checklist was completed for this revision which should have identified the procedure discrepancy. The individual who performed this checklist is no longer employed by Comed.
CORRECTIVE STEPS TAKEN AND RESULTS ACillEVED:
On November 12,1997, at 0900, PIF # Ql997-04352 was initiated as an NRC llPCI SOP 1 identified issue concerning inconsistencies in panel references within QCOP 2300-08. The immediate action was to have QCOP 2300-08 walked down and verified by a Senior Reactor Operator. A procedure change request was submitted on November 12,1997, to correct errors found. The procedure change request was processed and the corrected procedure became effective November 17,1997.
CORRECTIVE STEPS TAKEN TO AVOID FURTilER VIOLATIONS No further actions are required for this issue.
DATE WilEN FULL COMPLIANCE WAS ACillEVED:
Full compliance was met on November 17,1997, when the QCOP 2300-08, Revision i1, became efTective.
ATTACIIMENT A RESPONSE TO NOTICE OF VIOLATION
~
SVP-98-095
', (Page 2 of 7)
NOTICE OF VIOLATION (50-254(265)/97022-03) 10 CFR 50, Appendix B, Criterion III, " Design Control", requires, ia part, that design control measures assure that the design basis for structures, systems, and components are correctly translated into specifications.
Contrary to the above, as of November 12,1997, Modification M04-1(2)-91-013,
" Modify Break Detection Logic to Prevent Spurious Isolation of HPCl", an activity affecting quality, did not address the additional attemating current (AC) inboard isolation valve closure time during a loss of offsite power event. As a result, the overall inboard isolation valve closure time was not reviewed against the valve's design basis time assumed in the Updated Final Safety Analysis Report.
This is a Severity Level IV violation (Supplement 1). (50-254/97022-03; 50-265/97022-03)
REASON FOR Tile VIOLATION:
Comed accepts this violation.
The reason for this violation was failure to follow modification and safety evaluation procedures.
Specifically, the 10CFR50.59 safety evaluation failed to address all the effects of the modified HPCI valve isolation logic.
The original logic design for the HPCI containment isolation valves (MO-l(2)-2301-4 & 5) provided isolation signals from the AC and DC logic to both the inboard and outboard isolation valves. The nine second upper limit for the HPCI steamline high flow trip time delay is based on the initial analysis used for this isolation. This analysis assumed a steam break concurrent with a loss of offsite power and a failure of the outboard DC powered isolation valve. The inboard AC isolation valve would not move until the Diesel Generator (DG) started and loaded, which was assumed to take 13 seconds. Therefore, the nine second time delay would not preclude valve movement any longer than what was originally assumed in the design basis. This is because the DC logic timer would still time out and provide the isolation signal, and the inboard valve would close when AC power became available from the DG. The nine second limit was used based on historical starting time for the DG of 10 seconds.
In 1991, modification M04-l(2)-91-013 "HPCI Turbine Exhaust Sparger and External Vacuum Breaker Line" separated the power sources for the logic to the inboard and outboard isolation valves. (Please note the title clarification). After this modification, the AC logic provided a closure signal for the inboard AC valve and the DC logic provided a closure signal for the outboard DC valve. The AC time delay relay will not start until after the DG has loaded, and valve movement will not start until the relay has timed out. This effectively added 10 seconds (the time that it takes for an emergency diesel generator to start and load) to the closing time under the design basis analysis.
ATTACIIMENT A RESPONSE TO NOTICE OF VIOLATION SVP-98-095 (Page 3 of 7)
The modification package did not identify an evaluation of this change in the closure time for the inboard AC valve. This potential problem is documented in selfidentified Problem Identification Form #Q1997-04344. The issue screening prepared for the PIF detennined that the closure times remained within the Updated Final Safety Analysis Report criteria.
CORRECTIVE STEPS TAKEN AND RESULTS ACIIIEVED The effects of the longer valve closure times were evaluated in the issue screening prepared in response to Problem Identification Form #Q1997-04344 on November 14,1997. As agreed by the inspection committee, this evaluation determined that total valve closure time remained within the design basis allowables for the pressure / temperature effects and radiological effects as established in calculations QC-030-M-001, Revision 2 " Pressure / Temperature Transient Analysis for HPCI Line Steam Break in Torus Compartment" and the radiological zone maps based on Specification N202 Appendix A. Therefore, the Primary Containment System remains within the design basis allowable. A 10CFR50.59 will be prepared to address the logic changes associated with modifications. This will be tracked NTS # 254-100-97-02203.01 and will be complete hy April 30,1998.
CORRECTIVE STEPS TAKEN TO AVOID FURTilER VIOLATION Site Engineering has performed a formal root cause investigation on the quality concerns with 10CFR50 59 safety evaluations. The investigation determined the root cause to be a progranmutic weakness in the imple.nentation of the 50.59 process as indicated by:
. The lack of a clear understanding of responsibilities by the preparers and reviewers.
- The lack of knowledge on the tools and references related to the design and bcensing basis of the station.
Site Engineering has issued a 50.59 safety evaluation responsibilities document to all qualified preparers and reviewers as interim guidance. This action is complete.
Perfornunce based training has been initiated for the preparers and reviewers of 50.59 safety evaluations. This activity is being tracked in NTS item 254-100-97-02203.03, which is due August 30,1998. This training, in the form of a two-day workshop, focuses on the 50.59 j process, and the expectations and responsibilities for the preparers and reviewers.
Additionally, training will be provided in Modifications and Lessons Learned that will address logic changes associated with design changes. This activity will be tracked by NTS # 254-100-97-02203.02 and will be complete by July 1,1998.
DATE WilEN FULL COMPLIANCE WILL BE ACillEVED Full compliance will be achieved on April 30,1998. (NTS #254 100-97-02203.01, due date April 30,1998.)
1
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ATTACHMENT A RESPONSE TO NOTICE OF VIOLATION SVP-98-095
. (Page 4 of 7)
NOTICE OF VIOLATION (50-254/97022-04a & 50-254/97022-04b) 10CFR50, appendix B, Criterion V. " Instructions, Procedures and Drawings," requires that activities affecting quality shall be prescribed by documented procedures of a type appropriate to the circumstances and shall be accomplished in accordance with these procedures.
B. Nuclear Station work Procedure No NSWP-A-04,"10 CFR Safety Evaluation Process", stated, in part, that previously performed screenings can fulfdl the screening requirement provided they meet the validation criteria of Exhibit 11, " Validation of Previously Performed Safety Evaluations and Screenings," to determine in the existing screening remains valid.
Contrary to the above, (1) The 10CFR 50.59 screening approved on January 26,1996, for temporary alteration No 96-1-005, " Fine Tune llPCI Flow Controller at Direction of system Engineer,"
an activity affecting quality, evaluated the installation of a recorder to monite six (6) HPCI process parameters. However, the work request that installed the recorder also installed additional instrumentation. This instrumentation was not evaluated t -
Exhibit H to determine if the existing screening remained valid.
(2) The 10 CFR 50.59 screening approved on February 28,1996, for temporary alteration No. 96-1-063, " Connect chart Recorder to HPCI Oil Pressure Switches to Monitor Pressure during QIR14. " and activity affecting quality, evaluated the installation of a recorder to monitor ifPCI process parameters. However the work request that installed the recorder also installed additional instrumentation. This instrumentation was not evaluated by Exhibit H to determine if the existing screening remained valid.
This is a Severity Level IV violation (Supplement 1)
ATTACIIMENT A RESPONSE TO NOTICE OF VIOLATION
' ~
SVP-98-095
, (Page 5 of 7)
REASON FOR Tile VIOLATION Comed accepts this violation.
(50-254/97022-04a) Temporary Alteration (TA) 96-1-005 was issued to install test equipment on the HPCI system. The screening as issued was consistent with and evaluated the items installed under the TA process. The Engineering Request (ER) 9600131 that initiated the TA included the request to add the Linear Variable Differential Transformers (LVDTs). Inclusion of these instruments in the TA and the screening was not required. Installation of these types of instruments is allowed under QAP 0300-12 since they do not require a system breach, have no electrical connections, perform no component alteration and steps were included in the work package for installation and removal. The pressure gauges were installed when the HPCI system had been declared inoperable due to a problem found during the conduct of the testing under the TA. Use of the troubleshooting procedure in existence at the time of the work was listed as a step in the work instructions. As the HPCI system was inoperable at the time of use of these gauges, inclusion in the TA paperwork was not necessary. After troubleshooting was completed and repairs were made, these gauges were removed, the system was returned to senice (RTS) and use of the TA continued.
(50-254/97022-04b) Temporary Alteration (TA) 96-1-63 was issued to install test equipment on the HPCI system. The equipment in the TA documentation consisted of a chart recorder and a validyne. The 50.59 screening only addressed the chart recorder installation and did not address the use of the validyne. This was a result of a lack of attention to detail when preparing and reviewing the TA and the 50.59 screening.
This is an example of an inadequate screening, as not all of the equipment being installed by the TA was described in the 50.59 safety screening. The procedure in use at the time of the TA installation was QCAP 1100-9, Revision 3. With this procedure there was no option to validate a previous screening. Ifit had been identified that additional instruments should have been evaluated, a new screening would have been required to supplement or replace the original screening.
CORRECTIVE STEPS TAKEN AND RESULTS AClllEVED PlFs Q1997-039813982,4468, and 4500 were written to address the above issues. Both TAs are no longer installed in the plant. Revision of the 50.59 screening for TA 96-1-63 is not required.
i
ATTACllMENT A RESPONSE TO NOTICE OF VIOLATION
~
SVP-98-095
. (Page 6 of 7)
CORRECTIVE STEPS TAKEN TO PREVENT FURTIIER VIOLATION The following corrective action has been initiated to ensure that this situation does recur:
- 1. See corrective action for violation 50-254 & 265/97022-03.
(NTS item 254-100-97-02203.03, due August 30,1998.)
DATE WIIEN FULL COMPLIANCE WAS ACillEVED Full compliance was achieved when the temporary alteration 96-1-63 was removed on April 23,1996.
}
ATTACHMENT A RESPONSE TO NOTICE OF VIOLATION l SVP-98-095
'~
. (Page 7 of 7)
NOTICE OF VIOLATION (50-254(265)/97022-06) 10 CFR 50, Appendix B, Criterion V. " Instructions, Procedures and Drawings," requires that activities affecting quality shall be prescribed by documented procedures of a type appropriate to the circumstances and shall be accomplished in accordance with these procedures.
C. Quad Cities procedure NSWP-A-04, Rev. O, "10 CFR Safety Evaluation Process," Section 5.4.1.3 states, in part, that the report to the NRC shall contain a brief description of each change, test, or experiment and a sununary of the safety evaluation performed.
Contrary to the above, on July 1996 and October 1997 the 10 CFR 50.59 summary reports submitted to the NRC contained only those 50.59 descriptions that changed the Updated Final Safety Analysis Report (UFSAR) and not a description of each change, test, and experiment performed at the facility.
This is a Severity Level IV violation (Supplement 1). (50-254/97022-06; 50-265/97022-06)
REASON FOR Tile VIOLATION:
Comed accepts this violation.
The cause of failure to submit all SEs to the NRC was based upon an improper management decision in 1995 to not transmit those SEs that were not directly related to changes to the facility, as described in the UFSAR.
CORRECTIVE STEPS TAKEN AND RESULTS ACillEVED:
- 1. A review of all SEs, not submitted in the 1995 and 1996 SE summary report, was completed.
- 2. Appropriate personnel have been briefed on the importance of an accurate accounting of all SEs designated for transmittal to the NRC.
- 3. Applicable SEs, not previously submitted, will be submitted to the NRC by March 31,1998.
(NTS item 254-180-97-SCAQ0002401, due March 31,1998.)
CORRECTIVE STEPS TAKEN TO AVOID FURTilER VIOLATIONS
- 1. Revised procedure QCAP 0500-01 " Processing 10CFR50.59 Safety Evaluations", to specify that all 50.59 evaluations are to be included in the 50.59 Summary Report sent to the NRC. This was completed on January 29,1998,
)
DATE WilEN FULL COMPLIANCE WILL BE ACillEVED:
Full compliance wiii be met on March 31,1998, when the applicable SEs are submitted to the NRC, (NTS item 254-180-97-SCAQ0002401, due March 31,1998.)
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