IR 05000400/2008002

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IR 05000400-08-002 on 01/01/2008 - 03/31/2008 for Shearon Harris, Unit 1; Routine Integrated Report
ML081130049
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 04/21/2008
From: Randy Musser
NRC/RGN-II/DRP/RPB4
To: Duncan R
Carolina Power & Light Co
References
IR-08-002
Download: ML081130049 (22)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION REGION II SAM NUNN ATLANTA FEDERAL CENTER 61 FORSYTH STREET, SW, SUITE 23T85 ATLANTA, GEORGIA 30303-8931 April 21, 2008 Carolina Power and Light Company ATTN: Mr. Robert J. Duncan, II Vice President - Harris Plant Shearon Harris Nuclear Power Plant P. O. Box 165, Mail Code: Zone 1 New Hill, North Carolina 27562-0165

SUBJECT: SHEARON HARRIS NUCLEAR POWER PLANT - NRC INTEGRATED INSPECTION REPORT 05000400/2008002

Dear Mr. Duncan:

On March 31, 2008, the US Nuclear Regulatory Commission (NRC) completed an inspection at your Shearon Harris reactor facility. The enclosed integrated inspection report documents the inspection findings, which were discussed on April 2, 2008 with you and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the results of this inspection, no finding s of significance were identified by the NRC. However, one licensee identified violation is listed in Section 4OA7 of this report. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section VI.A.1 of the NRC Enforcement Policy because of its very low safety significance and because it is entered into your corrective action program. If you contest this non-cited violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Shearon Harris facility.

In accordance with 10 CFR 2.390 of the "NRC's Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document CP&L 2Room or from the Publicly Available Records (PARS) components of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html http://www.nrc.gov/NRC/ADAMS/index.html.

(the Public Electronic Reading Room).

Sincerely,

/RA/ Randall A. Musser, Chief Reactor Projects Branch 4

Division of Reactor Projects Docket No.: 50-400 License No.: NPF-63

Enclosure:

NRC Inspection Report 05000400/2008002 w/Attachment: Supplemental Information

REGION II==

Docket No:

50-400 License No:

NPF-63 Report No:

05000400/2008002 Licensee: Carolina Power and Light Company Facility: Shearon Harris Nuclear Power Plant, Unit 1 Location: 5413 Shearon Harris Road New Hill, NC 27562 Dates: January 1, 2008 through March 31, 2008 Inspectors:

P. O'Bryan, Senior Resident Inspector M. King, Resident Inspector R. Rodriguez, Senior Reactor Inspector, Section 4OA3 S. Walker, Senior Reactor Inspector, Section 4OA5 C. Even, Reactor Inspector, Sections 1R05 and 1R19 J. Austin, Senior Resident Inspector, Sections 1R05 and 1R19 Approved by:

R. Musser, Chief Reactor Projects Branch 4 Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000400/2008-002; January 1, 2008

- March 31, 2008; Shearon Harris Nuclear Power Plant, Unit 1; Routine Integrated Report.

The report covered a three-month period of inspection by resident inspectors and announced inspection by regional operator licensing inspectors. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.

A. Inspector-Identified and Self-Revealing Findings

None

B. Licensee-Identified Violations

A violation of very low safety significance, which was identified by the licensee, has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. This violation and its corrective action tracking number is listed in Section 40A7 of this report.

REPORT DETAILS

Summary of Plant Status

The unit began the inspection period at rated thermal power, and operated at or near full power for the entire inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R04 Equipment Alignment

a. Inspection Scope

Partial System Walkdowns:

The inspectors performed the following three partial system walkdowns, while the indicated structures, systems and components (SSCs) were out-of-service (OOS) for maintenance and testing:

  • A essential services chilled water train with the B essential services chilled water train out-of-service on January 17, 2008.
  • B charging and safety injection train with A charging and safety injection train out-of-service on February 9, 2008.

To evaluate the operability of the selected trains or systems under these conditions, the inspectors reviewed valve and power alignments by comparing observed positions of valves, switches, and electrical power breakers to the procedures and drawings listed in the Attachment.

Complete System Walkdown:

The inspectors conducted a detailed review of the alignment and condition of the auxiliary feed water system. To determine the proper system alignment, the inspectors reviewed the procedures, drawings, and Final Safety Analysis Report (FSAR) sections listed in the Attachment.

The inspectors walked down the system, to verify that the existing alignment of the system was consistent with the correct alignment. Items reviewed during the walkdown included the following:

  • Valves are correctly positioned and do not exhibit leakage that would impact the function(s) of any given valve.
  • Electrical power is available as required.

4* Major system components are correctly labeled, lubricated, cooled, ventilated, etc.

  • Hangers and supports are correctly installed and functional.
  • Essential support systems are operational.
  • Ancillary equipment or debris does not interfere with system performance.
  • Tagging clearances are appropriate.
  • Valves are locked as required by the licensee's locked valve program.

The inspectors reviewed the documents listed in the Attachment, to verify that the ability of the system to perform its function could not be affected by outstanding design issues, temporary modifications, operator workarounds, adverse conditions, and other system-related issues tracked by the Engineering Department.

The inspectors reviewed the following ARs associated with this area to verify that the licensee identified and implemented appropriate corrective actions:

  • AR #235850, T&T Valve Dimension on 1364 DWG not the Same as in CM-M0213
  • AR #237239, AFW Pump "A" Increased Vibration During Perf of OST-1211

b. Findings

No findings of significance were identified.

1R05 Fire Protection

a. Inspection Scope

For the 21 areas identified below, the inspectors reviewed the licensee's control of transient combustible material and ignition sources, fire detection and suppression capabilities, fire barriers, and any related compensatory measures, to verify that those items were consistent with final safety analysis report (FSAR) Section 9.5.1, Fire Protection System, and FSAR Appendix 9.5.A, Fire Hazards

Analysis.

The inspectors walked down accessible portions of each area and reviewed results from related surveillance tests, to verify that conditions in these areas were consistent with descriptions of the applicable FSAR sections.

Documents reviewed are listed in the

.

  • 286' level of the reactor auxiliary building including areas 1-A-CSRA, 1-A-CSRB, and 1-A-ACP (3 areas)
  • A emergency diesel generator complex including areas 1-D-1-DGA-RM, 1-D-3-DGA-ES, 1-D-DTA, 1-D-1-DGA-ASU, 1-D-1-DGA-ER, and 1-D-3-DGA-HVR (6 areas)
  • 305' elevation of the reactor auxiliary building including the following areas: 12-A-CRC1, 12-A-HV&IR (2 areas)
  • 236' elevation of the reactor auxiliary building including the area 1-A-BAL-A (1 area)

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures

a. Inspection Scope

Internal Flooding The inspectors walked down the 190', 216', and the 286' elevations of the reactor auxiliary building, which are below flood levels or otherwise susceptible to flooding from postulated pipe breaks, to verify that the area configuration, features, and equipment functions were consistent with the descriptions and assumptions used in FSAR section 3.6A.6, Flooding Analysis, and in the supporting basis documents listed in the

. The inspectors reviewed the operator actions credited in the analysis, to verify that the desired results could be achieved using the plant procedures listed in the

.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification

a. Inspection Scope

On February 13, 2008, the inspectors observed licensed-operator performance during licensed operator continuing simulator training for crew E, to verify that operator performance was consistent with expected operator performance, as described in Exercise Guide EOP-sim-17.77. This training tested the operators' ability to respond to a large break loss-of-coolant accident. The inspectors focused on clarity and formality of communication, the use of procedures, alarm response, control board manipulations, group dynamics and supervisory oversight.

The inspectors observed the post-exercise critique to verify that the licensee had identified deficiencies and discrepancies that occurred during the simulator training.

b. Findings

No findings of significance were identified.

6 1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed two degraded SSC/function performance problems or conditions listed below to verify the licensee's handling of these performance problems or conditions in accordance with 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, and 10 CFR 50.65, Maintenance Rule. Documents reviewed are listed in the

.

  • Possible stem/disk separation for valve 1MS-231
  • Adjustments required to 1CT-118 and 1CT-119 during surveillance testing of the containment spray system The inspectors focused on the following attributes:
  • Appropriate work practices,
  • Identifying and addressing common cause failures,
  • Characterizing reliability issues (performance),
  • Charging unavailability (performance),
  • Trending key parameters (condition monitoring),
(1) or (a)
(2) classification and reclassification, and
  • Appropriateness of performance criteria for SSCs/functions classified (a)
(2) and/or appropriateness and adequacy of goals and corrective actions for SSCs/functions classified (a) (1).

The inspectors reviewed the following ARs associated with this area to verify that the licensee identified and implemented appropriate corrective actions:

  • AR #260360, Possible Stem/Disk Separation for Valve 1MS-231
  • AR #260827, OST-1118 Required Adjustment to 1CT-118
  • AR #267361, OST-1119 Required Adjustment to 1CT-119

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the licensee's risk assessments and the risk management actions for the plant configurations associated with the five activities listed below. The inspectors verified that the licensee performed adequate risk assessments, and implemented appropriate risk management acti ons when required by 10 CFR 50.65(a)7(4). For emergent work, the inspectors also verified that any increase in risk was promptly assessed, and that the appropriate risk management actions were promptly implemented.

  • Emergent corrective maintenance on air handler AH-10 on January 14, 2008.
  • Planned maintenance on the B essential services chiller on February 21, 2008.
  • Tornado Watch issued by National Weather Service on March 4, 2008.
  • Planned maintenance on A charging and safety injection pump with A emergency diesel generator ventilation fan A out of service on March 6, 2008.
  • Planned maintenance requiring opening the Cape Fear feeder to the A start-up transformer on March 26, 2008.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed five operability determinations addressed in the ARs listed below. The inspectors assessed the accuracy of the evaluations, the use and control of any necessary compensatory measures, and compliance with the TS

. The inspectors verified that the operability determinations were made as specified by Procedure OPS-NGGC-1305, Operability Determinations. The inspectors compared the justifications made in the determination to the requirements from the TS, the FSAR, and associated design-basis documents, to verify that operability was properly justified and the subject component or system remained available, such that no unrecognized increase in risk occurred:

  • AR #264717, A ESW Pump and Screen Wash Pump Inoperable Based on OST-1214 Data
  • AR #265528, B Chiller Pre-rotational Vane Actuator Linkage Out of Position
  • AR #267026, B Chiller Hot Gas Bypass Valve Actuator Found with Excessive Travel

b. Findings

No findings of significance were identified.

8 1R18 Plant Modifications

a. Inspection Scope

The inspectors reviewed the modification described in Engineering Change 68821, Flanged Cooling Coils in Containment Air Cooler AH-3, to verify that:

  • this modification did not degrade the design bases, licensing bases, and performance capabilities of risk significant SSCs,
  • implementing this modification did not place the plant in an unsafe condition, and
  • the design, implementation, and testing of this modification satisfied the requirements of 10 CFR 50, Appendix B.

b. Findings

No findings of significance were identified.

1R19 Post Maintenance Testing

a. Inspection Scope

For the five post-maintenance tests listed below, the inspectors witnessed the test and/or reviewed the test data, to verify that test results adequately demonstrated restoration of the affected safety function(s) described in the FSAR and TS. The tests included the following:

  • OST-1076, Auxiliary Feedwater Pump 1B-SB Operability Test Quarterly Interval following replacement of B train electrical circuit breaker on January 16, 2008.
  • OPT-1512, Essential Chilled Water Turbopak Units Quarterly Inspection/Checks after troubleshooting the ESCW Chiller temperature control module on January 17, 2008.
  • Operation test of valve 1CS-261 after corrective maintenance on January 22, 2008.
  • OST-1007, CVCS/SI System Operability Train A Quarterly Interval following maintenance to the A CSIP on February 9, 2008.
  • Execution of WO 01312515-01, 1B-ESW Motor Heater Relay and Ring Terminal Replacement on March 12, 2008.

The inspectors reviewed AR 248518248518 Adverse Trend of Valve 1AF-50 Stroke Time, to verify that the licensee identified and implemented appropriate corrective actions.

b. Findings

No findings of significance were identified.

9 1R22 Surveillance Testing

a. Inspection Scope

For the six surveillance tests identified below, the inspectors witnessed testing and/or reviewed test data, to verify that the systems, structures, and components involved in these tests satisfied the requirements described in the TS and the FSAR, and that the tests demonstrated that the SSCs were capable of performing their intended safety functions.

  • OST-1094, Sequencer Block Circuit and Containment Fan Cooler Testing Train A Quarterly Interval on January 2, 2008
  • MST-I0320, Train B Solid State Protection System Actuation Logic & Master Relay Test on January 15, 2008
  • OST-1045, ESFAS Train B Slave Relay Test Quarterly Interval on February 17, 2008 *
  • This procedure included inservice testing requirements.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA2 Identification and Resolution of Problems

.1 Routine Review of ARs

To aid in the identification of repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed frequent screenings of items entered into the CAP. The review was accomplished by reviewing daily AR reports.

4OA3 Event Follow-up

.1 (Closed) LER 05000400/2002004, Revs. 00-08 , Unanalyzed Condition Due to Inadequate Separation of Associated Circuits.

On December 20, 2002, upon inspection of the Safe Shutdown Analysis, the licensee identified that postulated fires could cause spurious actuation of certain valves. Valve actuation in the flowpath for the protected Charging/Safety Injection Pump could result in loss of the pump. Similarly, simultaneous spurious closure of multiple valves in the 10flowpaths to the Reactor Coolant Pump (RCP) seals could result in the loss of the RCP seal cooling. The licensee also identified other postulated fires which could cause spurious actuation of certain valves or components that could result in the conditions described above including transfer of Refueling Water Storage Tank inventory to the containment recirculation sump, transfer of some Reactor Coolant System (RCS)inventory to containment, inadvertent pressurizer spray, or potential impact to indication used to monitor RCS pressure and level. Revision 09 of this Licensee Event Report (LER) is a revision to a previously submitted LER that describes an unanalyzed condition due to inadequate separation of associated circuits. Specifically, LER 2002-004-00, submitted on February 18, 2003; LER 2002-004-01, submitted on March 26, 2003; LER 2002-004-02, submitted on September 19, 2003; LER 2002-004-03, submitted on April 12, 2004; LER 2002-004-04, submitted on October 12, 2004; LER 2002-004-05, submitted on November 15, 2004; LER 2002-004-06, submitted on December 20, 2004; LER 2002-004-07, submitted on March 21, 2005; and LER 2002-004-08, submitted on September 20, 2005, described similar unanalyzed conditions. Therefore, revisions 00 through 08 are administratively closed to revision 09. Any subsequent concerns or issues will be evaluated pursuant review and assessment of LER 2002-004-09, and the licensee's transition from the current licensing basis to NFPA 805, "Performance Based Standard for Fire Protection," in accordance with 10 CFR 50.48 (c).

.2 (Closed) LER 05000400/2007-004-00, Bare Conductors on B Steam Generator Wide Range Level Barton Transmitter as Identified via 10 CFR Part 21 Process.

On October 19, 2007, while replacing connector assemblies in response to a 10 CFR Part 21 Nuclear Industry Advisory issued by PRIME Measurement and Nuclear Regulatory Commission Information Notice 2006-14, the licensee discovered bare conductors at the connector assembly of Barton transmitter LT-487 (B steam generator wide range level indication). This condition was identified by the manufacturer of the transmitter as a condition resulting from the manufacturing process. This connector assembly is required to provide a water-tight seal in the postulated harsh post-accident environment of the reactor containment building. Technical Specifications require LT-487 to be operable in modes 1, 2, and 3. Without a proper watertight seal, the transmitter may not have operated properly in an accident condition. Since the transmitter was installed during initial plant construction, the licensee reported this event as a condition prohibited by Technical Specifications. The licensee replaced the transmitter on October 19, 2007. The enforcement aspects of this finding are discussed in Section

4OA7 of this report.

.3 (Closed) LER 05000400/2007-005-00, B Train of Essential Services Chilled Water was Inoperable for a Period Longer than Allowed by Technical Specifications.

On November 5, 2007, while attempting to place the B essential services chilled water system chiller in service, the chiller tripped off-line due to low refrigerant pressure. The cause of the low pressure trip was a loss of refrigerant from the chiller to the chiller receiver tank. This receiver tank is used to temporarily store refrigerant during maintenance requiring the refrigerant to be evacuated from the chiller. The receiver is isolated from the chiller during normal operations by an isolation valve, 1CY-7. After 11maintenance was completed October 13, 2007, 1CY-7 was not completely shut and refrigerant slowly leaked from the chiller to the receiver tank. Eventually, the refrigerant pressure dropped below the level required for chiller operation. This event was determined to be a self-revealing non-cited violation (NCV) of Technical Specification 3.7.13 and of very low safety significa nce (Green). This NCV was previously documented and closed in NRC inspection report 05000400/2007005 as NCV 05000400/2007005-01.

.4 Derailment of Train Cars During Movement of Spent Fuel

a. Inspection Scope

.

The inspectors responded to the site owner-controlled area when two cars of a train carrying spent reactor fuel from the Brunswick Nuclear Plant to the Shearon Harris Nuclear Plant derailed at the Shearon Harris Nuclear Plant on October 25, 2007. The inspectors observed the derailed train to ensure that there was no danger to the public health and safety or the environment. The inspectors also interviewed licensee personnel to gain an understanding of the event and assess follow-up actions, and reviewed the licensee's root cause investigation to assess the detail of review and adequacy of the root cause and proposed corrective actions.

The inspectors' investigation determined that, while transporting spent reactor fuel by train from the Brunswick Nuclear Power Plant to the Shearon Harris Nuclear Power Plant, the train's caboose derailed and the adjacent flat car partially derailed. The train cars derailed in the Shearon Harris owner controlled area and outside the protected area (PA) fence. The train approached the site in reverse and the cars derailed when they struck derailers that were installed on the tracks as security measures. The cars were set back on the train rails by railroad maintenance personnel on October 26, 2007.

Once the cars were back on the train tracks, the spent reactor fuel was transported into the Shearon Harris PA. The train tracks were not properly prepared prior to the approach of the train because of miscommunication between licensee operations personnel and site security personnel.

The inspectors also found that, while the train cars were derailed and during the transport of the spent reactor fuel, there was no danger to the public health and safety, or the environment.

b. Findings

No findings of significance were identified.

4OA5 Other Activities

.1 (Closed) URI 50-400/99-13-03: Adequacy of HEMYC Cable Wrap Fire Barrier Qualification Tests and Evaluations to Scope Installed Configurations.

Inspection Report 05000400/1999-13 documented the potential inadequacy of Hemyc fire barrier wrap material at Harris Nuclear Power Plant. The issue was unresolved 12pending further NRC review to determine whether the qualification tests of the Hemyc fire wrap systems were acceptable. In subsequent NRC fire tests, re sults indicated that Hemyc/MT materials could not be routinely relied upon as one hour fire barriers. The NRC staff has completed a significant effo rt informing industry of the concerns associated with these materials by issuing information notice (IN) 2005-07, Results of Hemyc Electrical Raceway Fire Barrier System Full Scale Fire Testing, and Generic

Letter (GL) 2006-03, Potentially Nonconforming Hemyc and MT Fire Barrier Configurations. As required by GL 2006-03, Harris Nuclear Power Plant has responded to the NRC concerns by identifying all applications of Hemyc/MT materials, implementing compensatory measures as appropriate, and initiating corrective actions to resolve as necessary. Based upon the licensee's letter of intent received by the NRC to transition the current licensing basis to NFPA 805 Performance Based Standard for Fire Protection in accordance with 10 CFR 50.48 (c), these compensatory measures will remain in place until a license amendment is approved by the NRC. Therefore, the NRC staff has determined this unresolved item (URI) is closed and any further evaluation of this issue will be conducted pursuant to review of the licensee's GL 2006-03 response and subsequent license amendment approval

4OA6 Meetings, Including Exit

On April 2, 2008, the resident inspectors presented the inspection results to Mr. Robert Duncan and other members of his staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection.

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meets the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

Technical Specification 3.3.3.6 requires that the B steam generator wide range level transmitter, LT-487, be operable or the plant be shutdown to hot standby with seven days. Contrary to this requirement, LT-487 was not operable since installation of the transmitter connector assembly during initial plant construction because the connector conductors were not properly insulated. Improper insulation of the conductors could have led to an electrical short circuit in the post-accident reactor containment building environment. This finding was determined to be of very low safety significance because alternate indications of adequate heat sink (narrow range steam generator level and auxiliary feedwater flow to the B steam generator) were available during an event which may have caused a harsh environment inside of the reactor containment building. For

events that would not cause a harsh environment inside the reactor containment building, LT-487 would function properly as evidenced by its satisfactory operation since it was installed during plant construction. Therefore, the B steam generator was available for core cooling. This event is documented in the licensee's corrective action

program as AR 221840221840

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

C. Burton, Director, Site Operations
D. Corlett, Supervisor, Licensing/Regulatory Programs
J. Dills, Manager, Outage and Scheduling
J. Dufner, Manager, Maintenance
R. Duncan, Vice President Harris Plant
M. Findlay, Superintendent, Security
W. Gurganious, Training Manager
K. Henderson, Plant General Manager
C. Kamiliaris, Manager, Nuclear Assessment Section
S. O'Connor, Manager, Engineering
J. Pierce, Supervisor, Nuclear Assessment
G. Simmons, Superintendent, Radiation Control
J. Warner, Manager, Operations

NRC personnel

R. Musser, Chief, Reactor Projects Branch 4

2

LIST OF ITEMS

OPEN, CLOSED AND DISCUSSED

Opened

None.

Closed

50-400/99-13-03

URI Adequacy of HEMYC Cable Wrap Fire

Barrier Qualification Tests and

Evaluations to Scope Installed

Configurations (Section 4OA5)

05000400/2002004-00

LER Unanalyzed Condition Due to

Inadequate Separation of Associated

Circuits. (Section 4OA3)

05000400/2002004-01

LER Unanalyzed Condition Due to

Inadequate Separation of Associated Circuits. (Section 4OA3)

05000400/2002004-02

LER Unanalyzed Condition Due to

Inadequate Separation of Associated Circuits. (Section 4OA3)

05000400/2002004-03

LER Unanalyzed Condition Due to

Inadequate Separation of Associated

Circuits. (Section 4OA3)

05000400/2002004-04

LER Unanalyzed Condition Due to

Inadequate Separation of Associated

Circuits. (Section 4OA3)

05000400/2002004-05

LER Unanalyzed Condition Due to

Inadequate Separation of Associated

Circuits. (Section 4OA3)

05000400/2002004-06

LER Unanalyzed Condition Due to

Inadequate Separation of Associated Circuits. (Section 4OA3)

05000400/2002004-07

LER Unanalyzed Condition Due to

Inadequate Separation of Associated Circuits. (Section 4OA3)

05000400/2002004-08

LER Unanalyzed Condition Due to

Inadequate Separation of Associated

Circuits. (Section 4OA3)

05000400/2007004-00

LER Bare Conductors on 'B' Steam

Generator Wide Range Level Barton

Transmitter as Identified via 10 CFR Part 21 Process (Section 4OA3)

05000400/2007005-00

LER 'B' Train of Essential Services Chilled

Water was inoperable for a period longer than allowed by Technical

Specifications (4OA3)

LIST OF DOCUMENTS REVIEWED