05000400/LER-2007-005

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LER-2007-005, 'B' Train of Essential Services Chilled Water was inoperable for a period longer than allowed by Technical Specifications
Harris Nuclear Plant - Unit 1
Event date: 11-5-2007
Report date: 1-4-2008
4002007005R00 - NRC Website

Energy Industry Identification System (EIIS) codes are identified in the text within brackets [ ].

I. DESCRIPTION OF EVENT

The plant was operating in mode 1 at 100% power at the time of the chiller trip. On 10/6/07 the 'B' chiller [CHU] of the ESCW system [KM] was shutdown for maintenance during Refueling Outage (RFO) 14. Part of the maintenance scope was to replace the compressor with a spare. The maintenance activities on the compressor required that the refrigerant be transferred to the receiver tank for temporary storage. Full refrigerant evacuation of 'B' chiller is an infrequent evolution that has been conducted less than five times since placing the Harris plant online in 1987. Prior to transferring the refrigerant to the receiver tank, the tank pressure boundary was checked per procedure. Based on entries from the RFO-14 ESCW project log, it is evident that the receiver tank held a vacuum from the time it was initially established on 5/16/07, indicating that there was no leakage at the receiver tank pressure boundary.

After completion of the maintenance, on 10/13/07, operations conducted a pressurized liquid transfer from the receiver tank to the turbopak. Following completion of the refrigerant transfer, the chiller refrigerant transfer valves were realigned to their operational position and independently verified. During the refrigerant transfer, 1CY-7 was not fully shut resulting in leakage of refrigerant from the turbopak to the receiver tank.

After all ESCW maintenance was completed in RFO-14 and the applicable clearances removed, the 'B' ESCW chiller was tested and restored to operable status. The post-maintenance testing performed at this time was inadequate to reveal that there was leakage past 1CY-7. The chiller was started and stopped several times during the 'B' safety train testing portion of RFO-14. After all 'B' safety train testing was completed, the 'B' ESCW chiller was run continuously from 11:50 on 10/20/07 to 09:55 on 10/23/07. On 10/23/07 at 09:55 the 'B' ESCW chiller was shutdown when the 'A' safety train was put in service during a scheduled safety train swap.

The next scheduled safety train swap was 11/5/07. During the train swap activities on 11/5/07, the 'B' ESCW chiller was started and tripped on low evaporator pressure after running for two minutes. During troubleshooting it was discovered that the receiver tank, which had been left empty at the completion of maintenance on 10/13/07, indicated Y4 full. Upon finding the 'B' ESCW chiller receiver tank 1/4 full, operations performed a valve line-up on the refrigerant transfer system boundary. During the valve line-up it was found that 1CY-7 could be turned approximately 1/16 to 1/8 turn farther in the shut direction.

At some time between 10/23/07 at 09:55 and 11/5/07 at 01:44, enough refrigerant had leaked from the turbopak to the receiver tank to render the chiller inoperable. The 'B' ESCW chiller was restored to an operable condition on 11/5/07 at 19:16. Based on available information, sufficient evidence does not exist to provide reasonable assurance that the 'B' ESCW chiller was operable at 01:44 on 11/2/07, 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> prior to the trip. The conclusion, therefore, is that the 'B' chiller was inoperable greater than the 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> allowed by Technical Specification 3.7.13 and that this condition is reportable under 10 CFR 50.73.a.2.i.B as a condition prohibited by Technical Specification. During the period of 10/23/07 through 11/5/07, the 'A' ESCW system was in service and fully functioning to supply all required loads. There was no other inoperable equipment at the time of the chiller trip that contributed to this event.

II. CAUSE OF EVENT

The root cause of this event is that the post-maintenance testing was not adequate to detect leakage of refrigerant to the receiver tank. The tests performed following this infrequent maintenance item were unable to detect the presence of leakage internal to the system from the turbopak to the receiver tank.

A contributing cause of this event was that the task to shut 1CY-7 was poorly performed by the non-licensed operator. There were no unusual characteristics of the work location that directly contributed to this event.

Another contributing cause was that there is no periodic monitoring of receiver tank level performed that would allow detection of refrigerant transfer leading to loss of chiller function.

III. SAFETY SIGNIFICANCE

The failure of the B ESCW chiller to start and run reliably prevented the 'B' train chiller from providing nominal 44 degree F inlet chilled water to cooling coils in the Air-Handling units associated with plant safety systems.

This condition is reportable under 10 CFR 50.73.a.2.i.B as a condition prohibited by Technical Specifications.

During the period of 10/23/07 through 11/5/07, the 'A' ESCW system was in operation and fully functioning to supply all required loads.

Potential Safety Consequences:

If a Design Basis Accident had occurred between 10/23/07 at 09:55 through 11/5/07 at 19:16, the 'B' ESCW train would not have been capable of performing its safety related functions. The corresponding consequences of having 'B' ESCW incapable of performing safety related functions are minimized by the existence of the 100% capacity redundant 'A' ESCW train. The 'A' ESCW train, which includes the 'A' chiller, was in service and fully functional during this time period.

IV. CORRECTIVE ACTIONS

The most practical means of preventing recurrence of the root cause of this failure is to revise two procedures to require an evacuation test of the receiver tank following refrigerant transfers. Successful completion of this test will ensure that leakage from the turbopak to the receiver will not occur.

There are three corrective actions to address the failure to fully shut 1CY-7. The first corrective action is to coach the individual responsible and all independent verifiers involved on expected performance and work practices. An additional corrective action is specified to revise the Operating Procedure to specify tight closure of 1CY-7 and to provide caution statements informing the operator of the consequences of leakage past 1CY- 7. The third corrective action is to brief the entire operations staff regarding the lessons learned from this investigation The corrective action to address the lack of monitoring is to revise the system Trending Basis Document to monitor receiver tank level once per day on Reactor Auxiliary Building (RAB) operator rounds. The RAB operator rounds will also be revised to add the monitoring requirement.

V. PREVIOUS SIMILAR EVENTS

There are two previous similar events that resulted in ESCW system being inoperable for a period longer than allowed by Technical Specifications. While the events are somewhat similar in nature, the corrective actions taken could not be expected to prevent an event such as the trip on 11/5/2007.