ML19321A089: Difference between revisions
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O VIRGINIA ELECTRIC AMD POWER COMPANY NORTH ANNA POWER STATION MONTHLY OPERATING REPORT | |||
' MONTH JUNE YEAR 1980 SUBMITTED: | |||
O | |||
VIRGINIA ELECTRIC AMD POWER COMPANY | |||
NORTH ANNA POWER STATION MONTHLY OPERATING REPORT | |||
' MONTH JUNE YEAR 1980 | |||
SUBMITTED: | |||
Ih r dll _ | Ih r dll _ | ||
SUPERIrligl0ENT - OPER%if.0?G y ' | SUPERIrligl0ENT - OPER%if.0?G y ' | ||
Line 36: | Line 25: | ||
+ | + | ||
0 | 0 | ||
_ STATION MAiiAGER | _ STATION MAiiAGER l | ||
l | |||
8007220Y3h | 8007220Y3h | ||
OPERATING DATA REPORT DOCKET NO. 50-338 DATE 7-9-80 COMPLETED BY W. R. Madison TELEPHONE (/03) 894-5151 - | OPERATING DATA REPORT DOCKET NO. 50-338 DATE 7-9-80 COMPLETED BY W. R. Madison TELEPHONE (/03) 894-5151 - | ||
't OPERATING STATUS | 't OPERATING STATUS North Anna Unit 1 N*''5 | ||
North Anna Unit 1 N*''5 | |||
: 1. Unit Name: | : 1. Unit Name: | ||
: 2. Reporting Period: | : 2. Reporting Period: | ||
Line 55: | Line 35: | ||
: 3. Licensed Thermal Power (MWt): | : 3. Licensed Thermal Power (MWt): | ||
2775 | 2775 | ||
: 4. Nameplate Rating (Gross MWe): | : 4. Nameplate Rating (Gross MWe): | ||
947 - ' ' ' | 947 - ' ' ' | ||
Line 65: | Line 44: | ||
: 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons: | : 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons: | ||
N/A | N/A | ||
: 9. Power Level To Which Restricted,If Any (Net MWe): N/A | : 9. Power Level To Which Restricted,If Any (Net MWe): N/A | ||
: 10. Reasons For Restrictions.If Any: N/A | : 10. Reasons For Restrictions.If Any: N/A This Month Yr to.Date Cumulative | ||
This Month Yr to.Date Cumulative | |||
: 11. Hours In Reporting Period 790 4.367 1R 1aa | : 11. Hours In Reporting Period 790 4.367 1R 1aa | ||
: 12. Number Of Hours Resctor Was Critical 634.8 3.494.6 11 659 R | : 12. Number Of Hours Resctor Was Critical 634.8 3.494.6 11 659 R | ||
Line 82: | Line 56: | ||
: 19. Unit Service Factor 83.2 75.6 73.6 | : 19. Unit Service Factor 83.2 75.6 73.6 | ||
: 20. Unit Availability Factor 63.2 75.6 73.6 | : 20. Unit Availability Factor 63.2 75.6 73.6 | ||
: 21. Unit Capacity Factor (Using MDC Net) | : 21. Unit Capacity Factor (Using MDC Net) 57.3 61.0 62.9 | ||
57.3 61.0 62.9 | |||
: 22. Unit Capscity Factor (Using DER Net) 56.8 60.4 62.3 | : 22. Unit Capscity Factor (Using DER Net) 56.8 60.4 62.3 | ||
: 23. Unit Forced Outage Rate 16.8 13.9 74 j 24. Shutdowns Scheduled Over Next 6 Months (Type. Date.and Duration of Each): .' | : 23. Unit Forced Outage Rate 16.8 13.9 74 j 24. Shutdowns Scheduled Over Next 6 Months (Type. Date.and Duration of Each): .' | ||
R9fnalinn- civ wnntee nnenmhnr 1980 and Januarv 1981. | R9fnalinn- civ wnntee nnenmhnr 1980 and Januarv 1981. | ||
: 25. If Shur Down At End Of Report Period. Estimated Date of Startup: N/A | : 25. If Shur Down At End Of Report Period. Estimated Date of Startup: N/A | ||
: 26. Units in Test Status (Prior to Commercial Operation): Forecast Achieved | : 26. Units in Test Status (Prior to Commercial Operation): Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION (9/77) | ||
INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION (9/77) | |||
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-338 UNIT NA'' | AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-338 UNIT NA'' | ||
DATE 7/9/80 COMPLETED BY W. R. Madison-TELEPHONE (703) 894-5151 MONTH JUNE, 1980 , | DATE 7/9/80 COMPLETED BY W. R. Madison-TELEPHONE (703) 894-5151 MONTH JUNE, 1980 , | ||
Line 101: | Line 70: | ||
(9/77) | (9/77) | ||
Page 1 of 2 DOCKET NO. 80-338 UNIT SHUTDOWNS AND POWER REDUCTIONS NA 1 UNIT NAME DATE 7/9/80 COMPLETED By W. R. Madienn REPORT MONTil June 1980 TELEPIIONE (70'd RQa R141 w. | Page 1 of 2 DOCKET NO. 80-338 UNIT SHUTDOWNS AND POWER REDUCTIONS NA 1 UNIT NAME DATE 7/9/80 COMPLETED By W. R. Madienn REPORT MONTil June 1980 TELEPIIONE (70'd RQa R141 w. | ||
, .5 ? 3 .E Licensee ,E t, Cause & Corrective No. Date g 3g ( .g g 5 Event ~g { Action to P | , .5 ? 3 .E Licensee ,E t, Cause & Corrective No. Date g 3g ( .g g 5 Event ~g { Action to P | ||
$E $ jgg Report # mO g Prevent Recurrence 6 | $E $ jgg Report # mO g Prevent Recurrence 6 | ||
80-13 This Shutdow1 was concluded on June 4 , 1980 at 1559 when the turbine generator was placed in service. | 80-13 This Shutdow1 was concluded on June 4 , 1980 at 1559 when the turbine generator was placed in service. | ||
Duration 88 lours . | Duration 88 lours . | ||
Line 117: | Line 83: | ||
_ _ _ _ _ __ - c _ _ _ | _ _ _ _ _ __ - c _ _ _ | ||
L j Page.2'of 2 DOCKET NO. 80-338 UNITSHUTDOWNS AND POWER REDUCTIONS NA 1 UNIT NAME DATE 7/4/An COMPLETED BY IJ - R- Ma rii enn REPORTMONTII JNE 1980 TEl,EPilONE . (703) 894-5151 n. | |||
L j | |||
Page.2'of 2 | |||
DOCKET NO. 80-338 UNITSHUTDOWNS AND POWER REDUCTIONS NA 1 UNIT NAME DATE 7/4/An COMPLETED BY IJ - R- Ma rii enn REPORTMONTII JNE 1980 TEl,EPilONE . (703) 894-5151 n. | |||
, .$ g 3 j' k Licensee ,E-r, % Cause & Corrective No. Date g -3 g i jgs Event p g'u8 Action to 5 mV 1- | , .$ g 3 j' k Licensee ,E-r, % Cause & Corrective No. Date g -3 g i jgs Event p g'u8 Action to 5 mV 1- | ||
$ j;5g Report # g Prevent Recurrence 5 | $ j;5g Report # g Prevent Recurrence 5 | ||
80-17 800618 F 6.4 A* 3 N/A N/A N/A Reactor trip due to a loose jumper in process rack no. 6. Jumper re-paired and reactor restarted. | 80-17 800618 F 6.4 A* 3 N/A N/A N/A Reactor trip due to a loose jumper in process rack no. 6. Jumper re-paired and reactor restarted. | ||
80-18 800626 F 15.9 H* 3 N/A N/A N/A Overtemperature AT reactor trip while calibrating N43 received a spurious spike on one of the other two channels. Trip setpoint checks were performed on the other two chan-nels. A faulty card was changed out in Channel II, test recorder install-ed and reactor was restarted. | 80-18 800626 F 15.9 H* 3 N/A N/A N/A Overtemperature AT reactor trip while calibrating N43 received a spurious spike on one of the other two channels. Trip setpoint checks were performed on the other two chan-nels. A faulty card was changed out in Channel II, test recorder install-ed and reactor was restarted. | ||
80-19 800627 F 2.7 A* N/A N/A N/A N/A Removed turbine generator from , | 80-19 800627 F 2.7 A* N/A N/A N/A N/A Removed turbine generator from , | ||
service due to B main steam trip valve air line broken. Repaired line and placed turbine generator back in service. | service due to B main steam trip valve air line broken. Repaired line and placed turbine generator back in service. | ||
I 2 3 4 F: Forced Reason: Method: Exhibit G. Instructions S: Scheduled A Equipment Failure (Explain) I-Manual for Preparation of Data | I 2 3 4 F: Forced Reason: Method: Exhibit G. Instructions S: Scheduled A Equipment Failure (Explain) I-Manual for Preparation of Data i B Maintenance of Test 2 Manual Scram. Entry Sheets for Licensee L C-Refueling 3 Automatic Scram. Event Report (LER) File (NURI'.G. | ||
i B Maintenance of Test 2 Manual Scram. Entry Sheets for Licensee L C-Refueling 3 Automatic Scram. Event Report (LER) File (NURI'.G. | |||
. D-Regulatory Restriction 4-Other (Explain) 0161) | . D-Regulatory Restriction 4-Other (Explain) 0161) | ||
E-Operator Training & Ucense Examinathm | E-Operator Training & Ucense Examinathm | ||
' F Administrative 5 | ' F Administrative 5 | ||
! G-Operational Error (Explain) Exhibit I Same Source | ! G-Operational Error (Explain) Exhibit I Same Source 19/77) - Il-Other (Explain) 9 | ||
19/77) - Il-Other (Explain) | |||
9 | |||
;s | ;s | ||
*See Attached Sheet. | *See Attached Sheet. | ||
Page 1 of- 1 . . ; | Page 1 of- 1 . . ; | ||
; | ; | ||
Line 154: | Line 104: | ||
; YEAR 1980 DATE July 11.1980 | ; YEAR 1980 DATE July 11.1980 | ||
! COMPLETED BY W. R. MADISON - | ! COMPLETED BY W. R. MADISON - | ||
[ 80-14'(H)6/6/80 Time: 1750. Decreased turbine power to 200 MWe to | [ 80-14'(H)6/6/80 Time: 1750. Decreased turbine power to 200 MWe to | ||
: perform secondary side Boric Acid Soak of the steam generators , | : perform secondary side Boric Acid Soak of the steam generators , | ||
l per 1-PT-72.4. This soak was performed per a Westinghouse recommen- | l per 1-PT-72.4. This soak was performed per a Westinghouse recommen- | ||
! dation in an attempt to minimize S/G tube denting. . | ! dation in an attempt to minimize S/G tube denting. . | ||
l-80-15 (G) 6/12/80' Time: 1847. An instrument technician was performing | l-80-15 (G) 6/12/80' Time: 1847. An instrument technician was performing 1-PT-44.4.1 (0verpressurization Protection Instrumentation Functional Test with PORV Operability Not Required) when he accidently opened | ||
1-PT-44.4.1 (0verpressurization Protection Instrumentation Functional | |||
Test with PORV Operability Not Required) when he accidently opened | |||
: the wrong switch in the protection and control racks. This l resulted in a steam flow / feed flow mismatch and low Channel I S/G level, causing a turbine trip / reactor trip. The periodic test s | : the wrong switch in the protection and control racks. This l resulted in a steam flow / feed flow mismatch and low Channel I S/G level, causing a turbine trip / reactor trip. The periodic test s | ||
was re. vised to clarify switch operation and the instrument technician was reinstructed. | was re. vised to clarify switch operation and the instrument technician was reinstructed. | ||
Line 171: | Line 115: | ||
reactor trip ~. The, card with the loose jumper was replaced. A random inspection of process cards will be performed to identify any other loose jumpers. | reactor trip ~. The, card with the loose jumper was replaced. A random inspection of process cards will be performed to identify any other loose jumpers. | ||
80-18 (H) 6/26/80 Time: 1422. . An instrument technician was calibrating N43 and a spurious spike occurred on one of the other two channels. This | 80-18 (H) 6/26/80 Time: 1422. . An instrument technician was calibrating N43 and a spurious spike occurred on one of the other two channels. This | ||
, resulted in a overtemperature AT reactor trip _. Subsequent to this | , resulted in a overtemperature AT reactor trip _. Subsequent to this trip setpoint checks were performed on both suspected channels with no defects or spikes noted. Prior to reactor startup a problem developed in Channel II and a faulty card was' changed out. Test recorders were installed and the reactor'was started up. The test recorder-indicated a fluctuating signal from the TAVE circuit for | ||
no defects or spikes noted. Prior to reactor startup a problem developed in Channel II and a faulty card was' changed out. Test | |||
recorders were installed and the reactor'was started up. The test recorder-indicated a fluctuating signal from the TAVE circuit for | |||
= | = | ||
Channel I. A faulty card was changed with no further problems noted. | Channel I. A faulty card was changed with no further problems noted. | ||
80-19. (A) 6/27/80 : Time,: 2315. ' Decreased power and took generator off-line , | 80-19. (A) 6/27/80 : Time,: 2315. ' Decreased power and took generator off-line , | ||
when a broken air line was discovered on one of the actuating , | when a broken air line was discovered on one of the actuating , | ||
Line 185: | Line 123: | ||
replaced and the generator placed on the 'line. Power was escalated to 100%. - | replaced and the generator placed on the 'line. Power was escalated to 100%. - | ||
l | l | ||
,.e-. .br .r, -<>-..e , +--r-- | ,.e-. .br .r, -<>-..e , +--r-- | ||
OPERATING DATA REPORT DOC n w. 50-339 DATE 7-9-80 COMPLETED BY W. R. Madison TELEPHONE ( 703) 894-5151 - | OPERATING DATA REPORT DOC n w. 50-339 DATE 7-9-80 COMPLETED BY W. R. Madison TELEPHONE ( 703) 894-5151 - | ||
OPERATING STATUS | OPERATING STATUS Notes | ||
Notes | |||
: 1. Unit Name: Nnrth Anna lin4+ 9 | : 1. Unit Name: Nnrth Anna lin4+ 9 | ||
: 2. Reporting Period: June 1980 Initial criticality achieved | : 2. Reporting Period: June 1980 Initial criticality achieved | ||
Line 208: | Line 139: | ||
N/A | N/A | ||
: 9. Power Level To Which Restricted,If Any (Net MWe): N/A | : 9. Power Level To Which Restricted,If Any (Net MWe): N/A | ||
: 10. Reasons For Restrictions.,1f Any: N/A | : 10. Reasons For Restrictions.,1f Any: N/A i | ||
This Month Yr. to.Date Cumulative | |||
,on | ,on | ||
: 11. Hours In Reporting Period ~/ ?ry 7?n | : 11. Hours In Reporting Period ~/ ?ry 7?n | ||
Line 225: | Line 154: | ||
~ | ~ | ||
: 21. Unit Capacity Factor (Using MDC Net) | : 21. Unit Capacity Factor (Using MDC Net) | ||
N/A N/A N/A | N/A N/A N/A | ||
: 22. Unit Capacity I actor (Using DER Net) N/A _ | : 22. Unit Capacity I actor (Using DER Net) N/A _ | ||
Line 232: | Line 160: | ||
: 24. Shutdowns Scheduled Over Next 6 Months (Type, Date,and Duration of Each): .' | : 24. Shutdowns Scheduled Over Next 6 Months (Type, Date,and Duration of Each): .' | ||
ti,/ 6 | ti,/ 6 | ||
. 25. If Shut Down At End Of Report Period, Estimated Date of Startup: N,/A | . 25. If Shut Down At End Of Report Period, Estimated Date of Startup: N,/A | ||
: 26. Units In Test Status (Prior to Commercial Operation): Forecast Achieved I | : 26. Units In Test Status (Prior to Commercial Operation): Forecast Achieved I | ||
INITIAL CRITICALITY ' 6/12/R0 INITIAL ELECTRICITY 7/27/R0 l COMMERCIAL OPERATION 9/4/80 19/77) m | INITIAL CRITICALITY ' 6/12/R0 INITIAL ELECTRICITY 7/27/R0 l COMMERCIAL OPERATION 9/4/80 19/77) m | ||
s . | s . | ||
AVERAGE DAILY UNIT POWER LEVEL | AVERAGE DAILY UNIT POWER LEVEL 50-339 DOCKET NO. | ||
50-339 DOCKET NO. | |||
UNIT NA 2 dan 7-9-80 , | UNIT NA 2 dan 7-9-80 , | ||
. <. COMPLETED BY W. R. Madison - | . <. COMPLETED BY W. R. Madison - | ||
TELEPHONE 03) 804- W | TELEPHONE 03) 804- W | ||
'MO TH June 1980 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POhER LEVEL (MWe-Net) (MWe-Net) | 'MO TH June 1980 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POhER LEVEL (MWe-Net) (MWe-Net) | ||
O 0 1 17 2 0. _ is 0 3 0 39 0 4 0 20 0 5 n 21 0 6 0 22 0 7 0 23 0 | O 0 1 17 2 0. _ is 0 3 0 39 0 4 0 20 0 5 n 21 0 6 0 22 0 7 0 23 0 8 0 24 0 9 0 25 0 10 0 26 0 | ||
8 0 24 0 9 0 25 0 10 0 26 0 | |||
1I 0 0 27 12 0 28 0 13 0 | 1I 0 0 27 12 0 28 0 13 0 | ||
29 . | 29 . | ||
14 0 3g 0 | 14 0 3g 0 15 0 3i 16 0 INSTRUCTIONS On this format list the average daily unit power levelin MWe Net for each day In the reporting month. Compute to the nearest whole megawatt. | ||
15 0 3i 16 0 INSTRUCTIONS On this format list the average daily unit power levelin MWe Net for each day In the reporting month. Compute to the nearest whole megawatt. | |||
(9/77) | (9/77) | ||
A a | A a | ||
DOCKET NO. R0 190 UNITSilUTDOWNS AND POWER REDUCTIONS UNIT NAME NA 2 i DATE 7-9-80 | DOCKET NO. R0 190 UNITSilUTDOWNS AND POWER REDUCTIONS UNIT NAME NA 2 i DATE 7-9-80 | ||
[- | [- | ||
COMPLETED BY W. R. Cartwricht REPORT MONT11 June 1980 | COMPLETED BY W. R. Cartwricht REPORT MONT11 June 1980 i - TELEPIlONE 1703) 894-5151 i | ||
i - TELEPIlONE 1703) 894-5151 i | |||
; . | ; . | ||
;, .$ ? 3g .E Licensee ,E t, h, Cause A Corrective No. Date g 3g .3 g A Event gg gO3 Actlim to F | ;, .$ ? 3g .E Licensee ,E t, h, Cause A Corrective No. Date g 3g .3 g A Event gg gO3 Actlim to F | ||
Line 277: | Line 185: | ||
o Prevent Recurrence | o Prevent Recurrence | ||
: j. - | : j. - | ||
2 Initial Electrical generatio-1 not achiev rd. | 2 Initial Electrical generatio-1 not achiev rd. | ||
i l - | i l - | ||
i i | i i | ||
i l | i l | ||
i 1 2 3 4 F: Forced Reason: Method: Exhibit G. instructions S: Scheduled A-Equipment Failure (Explain) I-Manus 1 for Preparation of Data B-Maintenance of Test 2-Manual Scram. Entry Sheets for Licensee C-Refueling 3-Automatic Scram. Event Report (LER) File (NURI.G. | i 1 2 3 4 F: Forced Reason: Method: Exhibit G. instructions S: Scheduled A-Equipment Failure (Explain) I-Manus 1 for Preparation of Data B-Maintenance of Test 2-Manual Scram. Entry Sheets for Licensee C-Refueling 3-Automatic Scram. Event Report (LER) File (NURI.G. | ||
D.!!egulatory Restriction 4 Other (Explain) 0161) 1 E-Operator Training & License Examination 1 F-Administ*:tive 5 | D.!!egulatory Restriction 4 Other (Explain) 0161) 1 E-Operator Training & License Examination 1 F-Administ*:tive 5 G Operatio tal i.tror (Explain) Exhibit I - Same Source 19/77) Il-Other (Explain)}} | ||
G Operatio tal i.tror (Explain) Exhibit I - Same Source 19/77) Il-Other (Explain)}} |
Revision as of 04:39, 1 February 2020
ML19321A089 | |
Person / Time | |
---|---|
Site: | North Anna |
Issue date: | 07/09/1980 |
From: | Wil Madison VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.) |
To: | |
Shared Package | |
ML19321A087 | List: |
References | |
NUDOCS 8007220436 | |
Download: ML19321A089 (9) | |
Text
- -
O VIRGINIA ELECTRIC AMD POWER COMPANY NORTH ANNA POWER STATION MONTHLY OPERATING REPORT
' MONTH JUNE YEAR 1980 SUBMITTED:
Ih r dll _
SUPERIrligl0ENT - OPER%if.0?G y '
APPROVED:
+
0
_ STATION MAiiAGER l
8007220Y3h
OPERATING DATA REPORT DOCKET NO. 50-338 DATE 7-9-80 COMPLETED BY W. R. Madison TELEPHONE (/03) 894-5151 -
't OPERATING STATUS North Anna Unit 1 N*5
- 1. Unit Name:
- 2. Reporting Period:
Ane 1980 ,
- 3. Licensed Thermal Power (MWt):
2775
- 4. Nameplate Rating (Gross MWe):
947 - ' ' '
- 5. Design Electrical Rating (Net MWe):
907
- 6. Maximum Dependable Capacity (Gross MWe):
920 7~. Maximum Dependable Capacity (Net MWe): 898
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
N/A
- 9. Power Level To Which Restricted,If Any (Net MWe): N/A
- 10. Reasons For Restrictions.If Any: N/A This Month Yr to.Date Cumulative
- 11. Hours In Reporting Period 790 4.367 1R 1aa
- 12. Number Of Hours Resctor Was Critical 634.8 3.494.6 11 659 R
- 13. Resetar Reserve Shutdown Hours 10.9 52.8 201.1
- 14. Hours Generator On.Line 598.9 3.301_9 11_qqq.1
- 15. Unit Reserve Shutdown Hours 0 0 0
- 16. Gross Thermal Energy Generated (MWH) l'.298.756 R 163 Al3 94 4a1 7ag
- 17. Gross Electrical Energy Generated (MWH) 398,487 _. 2.548.338 10.R9456R7
- 18. Net Electrical Energy Generated (MWH) 370,683 2,392.496 10.245.942
- 19. Unit Service Factor 83.2 75.6 73.6
- 20. Unit Availability Factor 63.2 75.6 73.6
- 21. Unit Capacity Factor (Using MDC Net) 57.3 61.0 62.9
- 22. Unit Capscity Factor (Using DER Net) 56.8 60.4 62.3
- 23. Unit Forced Outage Rate 16.8 13.9 74 j 24. Shutdowns Scheduled Over Next 6 Months (Type. Date.and Duration of Each): .'
R9fnalinn- civ wnntee nnenmhnr 1980 and Januarv 1981.
- 25. If Shur Down At End Of Report Period. Estimated Date of Startup: N/A
- 26. Units in Test Status (Prior to Commercial Operation): Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION (9/77)
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-338 UNIT NA
DATE 7/9/80 COMPLETED BY W. R. Madison-TELEPHONE (703) 894-5151 MONTH JUNE, 1980 ,
DAY AVERAGE MIL P WER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) 1 0 815 17 2 0 18 361 3 0 425 19 4
146 799 5 612 817 21 6 643 22 822 7 112 819
,- 23 8 140 24 816 9 184 25 823 to 387 491 26 1I 764 116 27 12 634 ,3 g7 13 0 29 814 14 635 810 30 15 802 3, 16 808 INSTRUCTIONS On this format, list the average daily unit power levelin MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.
(9/77)
Page 1 of 2 DOCKET NO.80-338 UNIT SHUTDOWNS AND POWER REDUCTIONS NA 1 UNIT NAME DATE 7/9/80 COMPLETED By W. R. Madienn REPORT MONTil June 1980 TELEPIIONE (70'd RQa R141 w.
, .5 ? 3 .E Licensee ,E t, Cause & Corrective No. Date g 3g ( .g g 5 Event ~g { Action to P
$E $ jgg Report # mO g Prevent Recurrence 6
80-13 This Shutdow1 was concluded on June 4 , 1980 at 1559 when the turbine generator was placed in service.
Duration 88 lours .
80-14 800606 S 87.7 H* N/A N/A N/A N/A Reduced turbine power to 200' mwd for Steam Generator secondary side Boric Acid Soak.
80-15 800612 F 8.1 G* 3 N/A N/A N/A Reactor trip due to operational error in operating wrong switch in protec-tion and control rack while perform-ing periodic test. Instrument tech-nician was instructed to be careful in switch operation. Reactor was restarted.
80-16 800614 F 6.0 A* N/A N/A N/A N/A Reduced reactor power to 40% to allow containment entry to repair LT-1474 (A S/G level) root valve. Repair valve and escalated to 100% power.
I 2 3 4 F: Forced Reason: Method: Exhibit G Instructions S: Scheduled A Equipment Failure (Explain) 1 -Manual .for Preparation of Data B-Maintenance of Test 2-Manual Scram. Entry Sheets for Licensee C-Refueling 3 Automatic Scram. Event Report (LER) File (NUREG-D-Regulatory Restriction 4-Other (Explain) 0161)
E-Operator Training & License Examination F-Administrative 5 6 G-Operational Error (Explain) Exhibit I Same Sourec (9/77) II-Other (Explain)
_ _ _ _ _ __ - c _ _ _
L j Page.2'of 2 DOCKET NO.80-338 UNITSHUTDOWNS AND POWER REDUCTIONS NA 1 UNIT NAME DATE 7/4/An COMPLETED BY IJ - R- Ma rii enn REPORTMONTII JNE 1980 TEl,EPilONE . (703) 894-5151 n.
, .$ g 3 j' k Licensee ,E-r, % Cause & Corrective No. Date g -3 g i jgs Event p g'u8 Action to 5 mV 1-
$ j;5g Report # g Prevent Recurrence 5
80-17 800618 F 6.4 A* 3 N/A N/A N/A Reactor trip due to a loose jumper in process rack no. 6. Jumper re-paired and reactor restarted.
80-18 800626 F 15.9 H* 3 N/A N/A N/A Overtemperature AT reactor trip while calibrating N43 received a spurious spike on one of the other two channels. Trip setpoint checks were performed on the other two chan-nels. A faulty card was changed out in Channel II, test recorder install-ed and reactor was restarted.
80-19 800627 F 2.7 A* N/A N/A N/A N/A Removed turbine generator from ,
service due to B main steam trip valve air line broken. Repaired line and placed turbine generator back in service.
I 2 3 4 F: Forced Reason: Method: Exhibit G. Instructions S: Scheduled A Equipment Failure (Explain) I-Manual for Preparation of Data i B Maintenance of Test 2 Manual Scram. Entry Sheets for Licensee L C-Refueling 3 Automatic Scram. Event Report (LER) File (NURI'.G.
. D-Regulatory Restriction 4-Other (Explain) 0161)
E-Operator Training & Ucense Examinathm
' F Administrative 5
! G-Operational Error (Explain) Exhibit I Same Source 19/77) - Il-Other (Explain) 9
- s
- See Attached Sheet.
Page 1 of- 1 . . ;
l' '
D UNIT SHUTDOWN AND POWER REDUCTI0tlS EXPLANATION SHEET DOCKET NO. 50-338 REPORT, MONTH' JUNE UNIT NAME North Anna i
- YEAR 1980 DATE July 11.1980
! COMPLETED BY W. R. MADISON -
[ 80-14'(H)6/6/80 Time: 1750. Decreased turbine power to 200 MWe to
- perform secondary side Boric Acid Soak of the steam generators ,
l per 1-PT-72.4. This soak was performed per a Westinghouse recommen-
! dation in an attempt to minimize S/G tube denting. .
l-80-15 (G) 6/12/80' Time: 1847. An instrument technician was performing 1-PT-44.4.1 (0verpressurization Protection Instrumentation Functional Test with PORV Operability Not Required) when he accidently opened
- the wrong switch in the protection and control racks. This l resulted in a steam flow / feed flow mismatch and low Channel I S/G level, causing a turbine trip / reactor trip. The periodic test s
was re. vised to clarify switch operation and the instrument technician was reinstructed.
80-16 (A) 6/14/80 Time: 1200. Decrease reactor power to 40% to al bw contain-ment entry to repair A S/G LT-1474 root valve. The root i..ve had a body to bonnet leak resulting in an erroneous level signal being sent to the protection circuit. The valve was firminited, leak stopped, and power was again escalated to 100%.
80-17'(A) 6/18/80 Time: 0905. An instrument technician was working in process rack no. 6. When.he completed his work he closed the rack door which jarred a loose jumper on a process card. This resulted in a steam flow / feed flow mismatch and A S/G low level causing a turbine trip /
reactor trip ~. The, card with the loose jumper was replaced. A random inspection of process cards will be performed to identify any other loose jumpers.
80-18 (H) 6/26/80 Time: 1422. . An instrument technician was calibrating N43 and a spurious spike occurred on one of the other two channels. This
, resulted in a overtemperature AT reactor trip _. Subsequent to this trip setpoint checks were performed on both suspected channels with no defects or spikes noted. Prior to reactor startup a problem developed in Channel II and a faulty card was' changed out. Test recorders were installed and the reactor'was started up. The test recorder-indicated a fluctuating signal from the TAVE circuit for
=
Channel I. A faulty card was changed with no further problems noted.
80-19. (A) 6/27/80 : Time,: 2315. ' Decreased power and took generator off-line ,
when a broken air line was discovered on one of the actuating ,
_ cylinders for B Main' Steam Trip ~ Valve. ' The broken air line was '
replaced and the generator placed on the 'line. Power was escalated to 100%. -
l
,.e-. .br .r, -<>-..e , +--r--
OPERATING DATA REPORT DOC n w. 50-339 DATE 7-9-80 COMPLETED BY W. R. Madison TELEPHONE ( 703) 894-5151 -
OPERATING STATUS Notes
- 1. Unit Name: Nnrth Anna lin4+ 9
- 2. Reporting Period: June 1980 Initial criticality achieved
- 3. LW Thermal Power (MWt): M9 on 6-12-80 at 2148.
~ '
~ -' '* '
- 4. Nameplate Rating (GrosiMWe): 947 -
- f. Design Electrical Rating (Nei MWe): 907
- 6. Maximum Dependable Capacity (Gross MWe): 928
- 7. Ma::! mum Dependable Capacity (Net MWe): 898
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
N/A
- 9. Power Level To Which Restricted,If Any (Net MWe): N/A
- 10. Reasons For Restrictions.,1f Any: N/A i
This Month Yr. to.Date Cumulative
,on
- 11. Hours In Reporting Period ~/ ?ry 7?n
- 12. Number Of Hours Reactor Was Critical 259 259 254
- 13. Resctor Reserve Shutdown Hours 0 0 0
- 14. Hours Generator On.Line 0 0 0 IS. Unit Reserve Shutdown Hours 0 0 n
- 16. Gross Thermal Energy Generated (MWH) 0 0 0
- 17. Gross Electrical Energy Generated (MWH) 0 , _ , ,
0 0
- 18. Net Electrical Energy Generated (MWH) . 0 0 __
0
- 19. Unit Service Factor N/A N/A N/A 2C Unit Availability Factor h/A N/A N/A
~
- 21. Unit Capacity Factor (Using MDC Net)
N/A N/A N/A
- 22. Unit Capacity I actor (Using DER Net) N/A _
N/A N/A
- 23. Unit Forced Outage Rare N/A N/A Nl/A
- 24. Shutdowns Scheduled Over Next 6 Months (Type, Date,and Duration of Each): .'
ti,/ 6
. 25. If Shut Down At End Of Report Period, Estimated Date of Startup: N,/A
- 26. Units In Test Status (Prior to Commercial Operation): Forecast Achieved I
INITIAL CRITICALITY ' 6/12/R0 INITIAL ELECTRICITY 7/27/R0 l COMMERCIAL OPERATION 9/4/80 19/77) m
s .
AVERAGE DAILY UNIT POWER LEVEL 50-339 DOCKET NO.
UNIT NA 2 dan 7-9-80 ,
. <. COMPLETED BY W. R. Madison -
TELEPHONE 03) 804- W
'MO TH June 1980 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POhER LEVEL (MWe-Net) (MWe-Net)
O 0 1 17 2 0. _ is 0 3 0 39 0 4 0 20 0 5 n 21 0 6 0 22 0 7 0 23 0 8 0 24 0 9 0 25 0 10 0 26 0
1I 0 0 27 12 0 28 0 13 0
29 .
14 0 3g 0 15 0 3i 16 0 INSTRUCTIONS On this format list the average daily unit power levelin MWe Net for each day In the reporting month. Compute to the nearest whole megawatt.
(9/77)
A a
DOCKET NO. R0 190 UNITSilUTDOWNS AND POWER REDUCTIONS UNIT NAME NA 2 i DATE 7-9-80
[-
COMPLETED BY W. R. Cartwricht REPORT MONT11 June 1980 i - TELEPIlONE 1703) 894-5151 i
- .
- , .$ ? 3g .E Licensee ,E t, h, Cause A Corrective No. Date g 3g .3 g A Event gg gO3 Actlim to F
$= 5 3 ;f, =g Report *r in O u
o Prevent Recurrence
- j. -
2 Initial Electrical generatio-1 not achiev rd.
i l -
i i
i l
i 1 2 3 4 F: Forced Reason: Method: Exhibit G. instructions S: Scheduled A-Equipment Failure (Explain) I-Manus 1 for Preparation of Data B-Maintenance of Test 2-Manual Scram. Entry Sheets for Licensee C-Refueling 3-Automatic Scram. Event Report (LER) File (NURI.G.
D.!!egulatory Restriction 4 Other (Explain) 0161) 1 E-Operator Training & License Examination 1 F-Administ*:tive 5 G Operatio tal i.tror (Explain) Exhibit I - Same Source 19/77) Il-Other (Explain)