ML19225B262: Difference between revisions
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{{#Wiki_filter:(/ //l | {{#Wiki_filter:(/ //l | ||
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* LICENSEE EVENT HEPORT | * LICENSEE EVENT HEPORT co .tnot at ocn. [_[ , | ||
co .tnot at ocn. [_[ , | |||
l } l l l@ | l } l l l@ | ||
(PLE ASE PHmT OH TYPt ALL HtOUtnf D INFOHMAliOM (h l Al Ll M Ml F 1 @l 0l 0 l -l 0 l 0 { 0 l 0 l 0 l - l 0 l Oj@! 411LICLfdE 14 L li! N ,' P. W. Jet 2 .' 7t. | (PLE ASE PHmT OH TYPt ALL HtOUtnf D INFOHMAliOM (h l Al Ll M Ml F 1 @l 0l 0 l -l 0 l 0 { 0 l 0 l 0 l - l 0 l Oj@! 411LICLfdE 14 L li! N ,' P. W. Jet 2 .' 7t. | ||
l 1 l T1Yl'E l 1JUl@lSJ LAI l l@ | l 1 l T1Yl'E l 1JUl@lSJ LAI l l@ | ||
Line 29: | Line 26: | ||
. $ [.Lj @ [ 0l 5l 0l 0 ! 0 l 3[_4 l 8 l@g6 ltu0ul t.7'l 7 l 9J@l0 rL 74 n-l 7HaouTuAIE l1 19 l 7 l9 l@ m3 i 6 c .i ui owe T um,. i .; i.; | . $ [.Lj @ [ 0l 5l 0l 0 ! 0 l 3[_4 l 8 l@g6 ltu0ul t.7'l 7 l 9J@l0 rL 74 n-l 7HaouTuAIE l1 19 l 7 l9 l@ m3 i 6 c .i ui owe T um,. i .; i.; | ||
t\ L".T D~0CIUP16CN Ar;c nic 'AULE CONStout% Cts h E.>J [ At 1020 on 6/7/79, radiation monitor R25A (Fue1 Sterace Pool Area. Gaseous Activity - l p -'O Lvent11ation system Isolation) was declared inoperable due to pump failure. Tech. Specj | t\ L".T D~0CIUP16CN Ar;c nic 'AULE CONStout% Cts h E.>J [ At 1020 on 6/7/79, radiation monitor R25A (Fue1 Sterace Pool Area. Gaseous Activity - l p -'O Lvent11ation system Isolation) was declared inoperable due to pump failure. Tech. Specj | ||
[njg l section 3.3.'..I and table 3.3.6 require.s a minimum of two radiation menitor channels o 1. I I to be cperable for the fuel storage area. Tech. Spec. 3.3.3.1 action statement l | [njg l section 3.3.'..I and table 3.3.6 require.s a minimum of two radiation menitor channels o 1. I I to be cperable for the fuel storage area. Tech. Spec. 3.3.3.1 action statement l l requirements were_ mt. r.25A was returned to an operable status at 1020 ot 6/15/79. l | ||
l requirements were_ mt. r.25A was returned to an operable status at 1020 ot 6/15/79. l | |||
[ c i. | [ c i. | ||
[o ; l The haalCh and safety of the public were not affected. l I | [o ; l The haalCh and safety of the public were not affected. l I | ||
Line 44: | Line 39: | ||
_., 21 22 2J 24 26 27 2d ACT:O' suTU=5 EFFE"? s % T *' ? ?. . A T1 Ac u 'J _ '. T t.P R D -4 PH1'.tE CO'P COVPONENT F O"*.1 du B MAN;.,F ACTUR E R TAM AC I W. Oi PL A'.T :T .~3 HOUR 5 SUU */i r T E D SU F P LI E R C LAGI ZI@ zlO; I zi@ l ol cl 01 l l sl@ lyjg Al@ lVl1l1l5j{ | _., 21 22 2J 24 26 27 2d ACT:O' suTU=5 EFFE"? s % T *' ? ?. . A T1 Ac u 'J _ '. T t.P R D -4 PH1'.tE CO'P COVPONENT F O"*.1 du B MAN;.,F ACTUR E R TAM AC I W. Oi PL A'.T :T .~3 HOUR 5 SUU */i r T E D SU F P LI E R C LAGI ZI@ zlO; I zi@ l ol cl 01 l l sl@ lyjg Al@ lVl1l1l5j{ | ||
3a , F- Ja . 3' 40 41 42 43 44 4; cAa: c :siplica ANo cc rem.t A:Tiow h i o l This event is attributable to purrp malfunction- The pump was repaired, belts l Egl replaced and the temparature overload devices reset. Following repair and verificatiop g , , . j [ o f pre;w r operat ion, 112 3.1 was declared operable at 1020 on 6/15/79. ] | 3a , F- Ja . 3' 40 41 42 43 44 4; cAa: c :siplica ANo cc rem.t A:Tiow h i o l This event is attributable to purrp malfunction- The pump was repaired, belts l Egl replaced and the temparature overload devices reset. Following repair and verificatiop g , , . j [ o f pre;w r operat ion, 112 3.1 was declared operable at 1020 on 6/15/79. ] | ||
1 3 l | 1 3 l | ||
' l 8 83 | ' l 8 83 | ||
Line 52: | Line 46: | ||
NA l l Alh! Operator observation . l | NA l l Alh! Operator observation . l | ||
, .m ,2 ., u <a y 80 fC. _ | , .m ,2 ., u <a y 80 fC. _ | ||
c | c | ||
.:'e A C TIVit Y LOCATION or RELE ASC | .:'e A C TIVit Y LOCATION or RELE ASC | ||
, n. tz J O Iz 13 = I l " l | , n. tz J O Iz 13 = I l " l | ||
, e ') , lg 41 4J bO F { '" r [ '. P '. . .~ . L a lt*. | , e ') , lg 41 4J bO F { '" r [ '. P '. . .~ . L a lt*. | ||
( .p'e**. | ( .p'e**. | ||
L,ij L..o LoIOjd,.z.'B,o | L,ij L..o LoIOjd,.z.'B,o | ||
Line 65: | Line 56: | ||
I.n e ' .h | I.n e ' .h | ||
/Th b07 | /Th b07 | ||
.. r ! ' C | .. r ! ' C 1 | ||
1 | |||
lol0l0l@l " | lol0l0l@l " | ||
NA - I | NA - I l | ||
l | |||
(. '.'m. - | (. '.'m. - | ||
,~ | ,~ | ||
9 @ @ O ' W~ | 9 @ @ O ' W~ | ||
>Ellz!D! . , | >Ellz!D! . , | ||
= 368 178 w | = 368 178 w | ||
1 | 1 | ||
"..i..,h " " " " | "..i..,h " " " " | ||
7007240 3 77 f_L] ! N. L._N^ l l I I I I I I l_! I l j_l a es sa ti . G. Hairston, III r. (205) 8_99--5156 | |||
7007240 3 77 | |||
f_L] ! N. L._N^ l l I I I I I I l_! I l j_l | |||
a es sa ti . G. Hairston, III r. (205) 8_99--5156 | |||
.- . ..}} | .- . ..}} |
Latest revision as of 03:45, 2 February 2020
ML19225B262 | |
Person / Time | |
---|---|
Site: | Farley |
Issue date: | 07/19/1979 |
From: | Hairston W ALABAMA POWER CO. |
To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
Shared Package | |
ML19225B252 | List: |
References | |
LER-79-027-03L, LER-79-27-3L, NUDOCS 7907240379 | |
Download: ML19225B262 (1) | |
Text
(/ //l
~
- LICENSEE EVENT HEPORT co .tnot at ocn. [_[ ,
l } l l l@
(PLE ASE PHmT OH TYPt ALL HtOUtnf D INFOHMAliOM (h l Al Ll M Ml F 1 @l 0l 0 l -l 0 l 0 { 0 l 0 l 0 l - l 0 l Oj@! 411LICLfdE 14 L li! N ,' P. W. Jet 2 .' 7t.
l 1 l T1Yl'E l 1JUl@lSJ LAI l l@
M d 's t i,, s t. ; s (v. I' (ovr Ej '
. $ [.Lj @ [ 0l 5l 0l 0 ! 0 l 3[_4 l 8 l@g6 ltu0ul t.7'l 7 l 9J@l0 rL 74 n-l 7HaouTuAIE l1 19 l 7 l9 l@ m3 i 6 c .i ui owe T um,. i .; i.;
t\ L".T D~0CIUP16CN Ar;c nic 'AULE CONStout% Cts h E.>J [ At 1020 on 6/7/79, radiation monitor R25A (Fue1 Sterace Pool Area. Gaseous Activity - l p -'O Lvent11ation system Isolation) was declared inoperable due to pump failure. Tech. Specj
[njg l section 3.3.'..I and table 3.3.6 require.s a minimum of two radiation menitor channels o 1. I I to be cperable for the fuel storage area. Tech. Spec. 3.3.3.1 action statement l l requirements were_ mt. r.25A was returned to an operable status at 1020 ot 6/15/79. l
[ c i.
[o ; l The haalCh and safety of the public were not affected. l I
o le l 7 E 9 'I 5 YS T E */ CAU3E CAUSE C O'.'P. valve CODE C c.'; E E ECOD CO*/ PD*.%T C?DE SUBCOpf s'>SCCDE 7
o 9 G
lB lB h lE lh I Xlh l P l U M l P I X l X lh l Hlh W h 9 10 11 12 . 13 18 19 20 SE oL'E N TI AL OCCURRENCE f;EFORT REVislON
,;p, EVE NT YEA 1
- REPCai N U. COoE TYPE N o.
O .hd ' ~ ' ' ' '
17 19 I l-l I o12I 7I I/l 1013I 23 i33Ll l-]
31 l_0j 32
_., 21 22 2J 24 26 27 2d ACT:O' suTU=5 EFFE"? s % T *' ? ?. . A T1 Ac u 'J _ '. T t.P R D -4 PH1'.tE CO'P COVPONENT F O"*.1 du B MAN;.,F ACTUR E R TAM AC I W. Oi PL A'.T :T .~3 HOUR 5 SUU */i r T E D SU F P LI E R C LAGI ZI@ zlO; I zi@ l ol cl 01 l l sl@ lyjg Al@ lVl1l1l5j{
3a , F- Ja . 3' 40 41 42 43 44 4; cAa: c :siplica ANo cc rem.t A:Tiow h i o l This event is attributable to purrp malfunction- The pump was repaired, belts l Egl replaced and the temparature overload devices reset. Following repair and verificatiop g , , . j [ o f pre;w r operat ion, 112 3.1 was declared operable at 1020 on 6/15/79. ]
1 3 l
' l 8 83
~Y_._ c.' rfric DCF s t'A ! [. *
.K;.r O!-E n 'a T A1 L S D::.CO' E *' Y DISCOVERY DESCf11PTIC'J 32 i
'., lsC lO l 0 l 0 l 0 P! '-
NA l l Alh! Operator observation . l
, .m ,2 ., u <a y 80 fC. _
c
.:'e A C TIVit Y LOCATION or RELE ASC
, n. tz J O Iz 13 = I l " l
, e ') , lg 41 4J bO F { '" r [ '. P '. . .~ . L a lt*.
( .p'e**.
L,ij L..o LoIOjd,.z.'B,o
. m N^
n ,wm g"pr M w I
I.n e ' .h
/Th b07
.. r ! ' C 1
lol0l0l@l "
NA - I l
(. '.'m. -
,~
9 @ @ O ' W~
>Ellz!D! . ,
= 368 178 w
1
"..i..,h " " " "
7007240 3 77 f_L] ! N. L._N^ l l I I I I I I l_! I l j_l a es sa ti . G. Hairston, III r. (205) 8_99--5156
.- . ..