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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046A4871993-07-23023 July 1993 LER 93-001-00:on 930607,determined RCP Uv & Underfrequency Portion of Rt Sys,& TDAFP Autostart Signal from RCP Bus Uv Contained Design Deviation Due to Personnel Error. Procedural Guidance enhanced.W/930723 Ltr ML20044D1331993-05-11011 May 1993 LER 91-007-01:on 910629,two Neutral Overcurrent Relays on Unit 1B Auxiliary Transformer Actuated,Resulting in Generator Trip & Reactor Trip.Caused by Electrical Fault. Loose Strand Removed from conductor.W/930511 Ltr ML20024G7191991-04-23023 April 1991 LER 91-001-00:on 910401,reactor Trip Occurred When Rod Dropped in Core.Caused by Defective Circuit Card in Rod Control Sys.Suspect Circuit Cards Replaced & Sent to Westinghouse for evaluation.W/910423 Ltr ML20043F1681990-06-0808 June 1990 LER 90-001-00:on 900512,reactor Tripped Due to lo-lo Water Level in Steam Generator 2A.Caused by Procedural Inadequacy. Procedure FNP-2-STP-151 Revised to Provide Addl Initial Conditions to Prevent Subj event.W/900608 Ltr ML20012D9591990-03-20020 March 1990 LER 90-002-00:on 900222,two Cases Found Where Surveillance Testing Procedures Did Not Perform All Tests Required by Tech Specs.Caused by Inadequate Procedural Guidance. Procedures revised.W/900320 Ltr ML20012C3031990-03-13013 March 1990 LER 90-001-00:on 900213,fire Watch Not Established within Required Time Period Due to Personnel Error.Administrative Procedure FNP-0-SOP-0.4 Revised & Personnel Retrained on requirements.W/900313 Ltr ML20012B4851990-03-0606 March 1990 LER 83-039/03X-2:on 830726,discovered That Handwheel for Inner Door of Personnel Airlock in Shut Position & Partially Opened.Caused by Excessive Use of Door During Outages.Door Repaired & Returned to Operable status.W/900306 Ltr ML19354E3341990-01-23023 January 1990 LER 89-016-00:on 891228,discovered That Required Surveillance for Plant Vent Stack Radioactive Gas Monitor Not Performed.Caused by Personnel Improperly Scheduling Surveillance for Time Later than Due date.W/900123 Ltr ML20011D5611989-12-18018 December 1989 LER 89-015-00:on 891118,reactor Tripped Due to Turbine Trip. Caused by Voltage Transient in Power Circuit to Digital electro-hydraulic Control Sys & Inverter Failure.Inverter Repaired & Returned to svc.W/891218 Ltr ML19332F9061989-12-13013 December 1989 LER 89-008-00:on 891113,containment Integrity Not Maintained for Approx 30 S.Caused by Personnel in That Inner Door Was Left Blocked Open.Personnel Counseled & Interim Administrative Controls established.W/891213 Ltr ML19332F6761989-12-12012 December 1989 LER 89-007-00:on 891112,both Motor Driven Auxiliary Feedwater Pumps Failed to Start Manually by Operator.Caused by Cognitive Personnel Error Re Design Change.Wiring Discrepancy Corrected & Pump Returned to svc.W/891212 Ltr ML19351A4571989-12-12012 December 1989 LER 89-014-00:from 891115-16,Tech Spec 3.0.3 Entered Voluntarily to Repair Leaking Containment Purge Isolation Dampers.Caused by Need to Repair Dampers.Dampers Closed & Automatic Isolation Feature restored.W/891212 Ltr ML19332F0851989-12-0707 December 1989 LER 89-006-00:on 891112,safety Injection & Reactor Trip Initiated Due to Low Steam Line Pressure.Caused by Personnel Error Involving Misconfiguration of Circuit Valve.Personnel Involved counseled.W/891207 Ltr ML19327C2621989-11-14014 November 1989 LER 89-012-00:on 891018,reactor Tripped Due to lo-lo Steam Generator Level Due to Closure of Governor Valves.Caused by Design Error in Digital electro-hydraulic Control Sys.Valve Position Limiter Feature removed.W/891114 Ltr ML19327C2671989-11-14014 November 1989 LER 89-013-00:on 891019,reactor Tripped Due to lo-lo Level in Steam Generator 2C.Caused by Operator Incorrectly Transferring Steam Generator Level Control to Main Feedwater.Involved Personnel counseled.W/891114 Ltr ML19354D4691989-11-0101 November 1989 LER 89-005-00:on 890930 & 1001,core Alterations Performed W/O Establishing Containment Refueling Integrity.Caused by Cognitive Personnel Error.Personnel Involved in Event Counseled.Containment Procedure strengthened.W/891101 Ltr ML19327B5451989-10-25025 October 1989 LER 89-011-00:on 890925,discovered That Tech Spec 4.6.3.1.a Surveillance Requirement Re Containment Air Lock Outer Door Not Done.Caused by Personnel Error.Individuals Involved Counseled Re Importance of Subj requirements.W/891025 Ltr ML19325D4941989-10-17017 October 1989 LER 89-004-00:on 890616,determined That Calculations Were Not Available to Demonstrate That Svc Water Sys Capable of Supplying Design Flow to safety-related Loads Under Scenario of Seismic event.W/891017 Ltr ML19325D2461989-10-12012 October 1989 LER 89-010-00:on 890920,reactor Tripped Manually Following Loss of Operating Steam Generator Feed Pump.Caused by Inadvertent Opening of Overspeed Trip Test Valve.Individual Involved in Event Counseled to Be More aware.W/891012 Ltr ML19325C7481989-10-10010 October 1989 LER 89-009-00:on 890525,determined That Power Range Nuclear Instrumentation Channels Reading Approx 7% Low.Equalizing Valves on Two of Three Instruments Were Leaking.Valves Repaired & Power Range Instruments adjusted.W/891010 Ltr ML20024F6841983-08-31031 August 1983 LER 83-031/03L-0:on 830806,during Testing,Instrumentation Channel Associated W/Level Transmitter LT-474 Declared Inoperable.Caused by Setpoint Drift of Comparator Card.Card Adjusted & Instrumentation Channel Declared Operable ML20024F6781983-08-31031 August 1983 LER 83-042/03L-0:on 830802,post-LOCA Hydrogen Recombiner 1A Declared Inoperable.Caused by Failure of Temp Indicator.New Indicator Installed & Declared Operable ML20024D0871983-07-26026 July 1983 LER 83-038/03L-0:on 830627,during Turbine Driven Auxiliary Feedwater Pump Inservice Test,Pump Failed to Start from Train a Steam Supply & Declared Inoperable.Caused by Valve HV-3226 Failing to Stroke properly.W/830726 Ltr ML20024C1251983-06-30030 June 1983 LER 83-027/03L-0:on 830607,during Performance of FNP-1-STP-43.0,train a Penetration Room Filtration Sys Declared Inoperable When Exhaust Fan Damper 3357A Would Not Open.Caused by Comparator Card failure.W/830630 Ltr ML20024C4011983-06-22022 June 1983 LER 83-025/03L-0:on 830528,during Calibr Procedure FNP-2-STP-612.0,reactor Coolant Pump 2A Undervoltage Relay 27-3 Declared Inoperable.Caused by Setpoint Drift.Relay Setpoint Adjusted ML20024C4061983-06-22022 June 1983 LER 83-024/03L-0:on 830525,following Increased Count Rate on Containment Atmosphere Particulate Monitoring Sys R-11, RCS Unidentified Leakage Found Above Tech Specs.Cause Not Stated.Loop B Drain Valve Tightened ML20023B5821983-04-29029 April 1983 LER 83-014/03L-0:on 830330,during Surveillance Test of Main Feedwater Pump Turbine 1A,RCS Tavg Decreased Below 541 F. Caused by Overfeeding of Steam Generators Due to Excessive Leak Past Main Feedwater Pump Discharge Valve ML20023B5281983-04-27027 April 1983 LER 83-015/03L-0:on 830328,instrumentation Channel Associated W/Steam Generator 1C Flow Transmitter FT-497 Declared Inoperable Due to Erroneous High Indication.Caused by Obstruction of Low Pressure Sensing Line.Line Cleared ML20023B5321983-04-27027 April 1983 LER 83-012/03L-0:on 830402,overtemp-delta Temp Loop 2 Channel II Declared Inoperable When Bistables 422C1-2 Tripped.Caused by Power Supply Failure of Comparator Card. Card Replaced & Loop Calibr ML20028G3051983-01-28028 January 1983 LER 82-062/03L-0:on 821231,noble Gas Activity Monitor R15 Declared Inoperable.Caused by Blown Fuse.Fuse Replaced & Monitor Returned to Svc ML20028G3111983-01-28028 January 1983 LER 83-001/03L-0:on 830102,RCS Subcooling Monitor Channel 2 Declared Inoperable Following Receipt of Main Control Board Alarms.Caused by Faulty Printed Circuit Card.Connector Pins on Card Cleaned ML20028G3091983-01-28028 January 1983 LER 82-063/03L-0:on 821230,B Train Chlorine Detector Declared Inoperable When Control Room Supply Damper Would Not Close.Caused by Faulty Solenoid Valve.Valve Replaced ML20027D9171982-11-0505 November 1982 LER 82-042/03L-0:on 821013,containment Auxiliary Personnel Hatch Failed to Meet Outer Door Acceptance Criteria.Caused by Worn Gaskets.Gaskets Replaced ML20027D3451982-10-26026 October 1982 LER 82-056/03L-0:on 820927,control Rod Bank D Declared Inoperable When Rods Would Not Move in Manual Control.Caused by Bank Select Relay Sticking,Causing Control Banks B & D to Be Selected Simultaneously.Relay Inspected & Reinstalled ML20027B7491982-09-21021 September 1982 LER 82-038/03L-0:on 820823,inboard & Outboard Pumps of Containment Atmosphere Monitors R-11 (Particulate Monitor) & R-12 (Gaseous Monitor) Declared Inoperable.Caused by Defective Relay & High Flow Switch.Relay & Switch Replaced ML20027B7471982-09-21021 September 1982 LER 82-036/03L-0:on 820824,2B Auxiliary Feedwater Pump Dc Control Power Breaker Inadvertently Opened.Caused by Personnel Error.Breaker Immediately Reclosed & Personnel Counseled ML20027B7461982-09-21021 September 1982 LER 82-051/03L-0:on 820823,1B Control Room Air Conditioner Failed,Rendering B Train Control Room Emergency Air Cleanup Sys Inoperable.Caused by Failed Fan Drive Belts.Belts Replaced & Sys Returned to Svc ML20027B7451982-09-21021 September 1982 LER 82-049/03L-0:on 820822,diesel Generator 1-2A Inadvertently Rendered Inoperable.Caused by Unauthorized Replacement of Lube Oil Strainers & Personnel Error. Generator Returned to Svc ML20052H6541982-04-30030 April 1982 LER 82-015/03L-0:on 820408,radiation Monitor 25A (Spent Fuel Storage Pool Area Gaseous activity-ventilation Sys Isolation) Declared Inoperable While Performing Test.Caused by Dirty Contacts on Mod Selector Switch.Contacts Cleaned ML20052H6591982-04-30030 April 1982 LER 82-017/03L-0:on 820413,FI-497 (Steam Generator 1C Feedwater Flow) Instrumentation Channel Declared Inoperable When Max Allowable Channel Check Error Was Exceeded.Caused by Faulty Transmitter Amplifier Card.Card Replaced ML20052C1391982-04-22022 April 1982 LER 82-014/03L-0:on 820326,28 & 0408,B Train Chlorine Detector Declared Inoperable Due to Detector Tape Not Advancing.Caused by Movement Indicator Binding Detector Tape & Sheared Pin in Tape Drive Mechanism ML20052C1371982-04-22022 April 1982 LER 82-014/03L-0:on 820328,while Performing Calibr & Functional Test,T average-low-low B Instrumentation Loop Declared Inoperable Due to Indicator Reading.Caused by Setpoint Drift.Power Supply Card Replaced ML20052C1401982-04-22022 April 1982 LER 82-015/03L-0:on 820325,radiation Monitor R29B Instrumentation Channel Declared Inoperable When Displays on All Readout Consoles Were Inaccurate.Caused by Dirty Contacts & Faulty Link.Contacts Cleaned ML20052C1351982-04-22022 April 1982 LER 82-012/03L-0:on 820326,during Routine Insp,Turbine Driven Auxiliary Feedwater Pump Declared Inoperable When Outboard Bearing Oil Bubbler Found Broken & Oil Drained. Possibly Caused by Workers Handling Scaffolding in Area ML20052A6571982-04-16016 April 1982 LER 82-013/03L-0:on 820317,containment Atmosphere Activity Monitors R-11 (Particulate Monitor) & R-12 (Gaseous Monitor) Declared Inoperable Due to Failure of Vacuum Pump.Caused by Failed Outboard Pump.Filter & Gasket Replaced ML20052A6671982-03-25025 March 1982 LER 82-009/03L-0:on 820228,instrumentation Loop Associated w/FT-474 (Steam Generator a Flow Transmitter) Declared Inoperable.Caused by Leaking Equalizing Valve.Valve Stem Repaired ML20052A6611982-03-25025 March 1982 LER 82-005/03L-0:on 820226,4160-volt B Train Ac Electrical Power Circuit Declared Inoperable When Emergency Bus 2G de-energized.Bus 2G de-energized When Breaker 2-DG15 Opened. Cause Under Investigation ML20052A6711982-03-25025 March 1982 LER 82-010/03L-0:on 820226,instrumentation Loop Associated w/LI-474 (Steam Generator a Level Indicator) Declared Inoperable.Caused by Loss of Necessary Level in Ref Leg While Steam Generator Not in Svc.Leg Refilled ML20052A6631982-03-25025 March 1982 LER 82-008/03L-0:on 820226,instrumentation Loop Associated w/LI-485 (Steam Generator B Level Indication) Declared Inoperable When Reading Was Out of Tolerance W/Other Channels.Caused by Obstruction in Ref Leg ML20050C1861982-03-19019 March 1982 LER 82-006/01T-0:on 820310,levels in Fire Protection Tanks a & B Fell to Approx 85,000 Gallons Each as Result of Inadvertent Actuation of Fire Protection Deluge Sys on Cooling Tower 1A.Caused by Personnel Error 1993-07-23
[Table view] Category:RO)
MONTHYEARML20046A4871993-07-23023 July 1993 LER 93-001-00:on 930607,determined RCP Uv & Underfrequency Portion of Rt Sys,& TDAFP Autostart Signal from RCP Bus Uv Contained Design Deviation Due to Personnel Error. Procedural Guidance enhanced.W/930723 Ltr ML20044D1331993-05-11011 May 1993 LER 91-007-01:on 910629,two Neutral Overcurrent Relays on Unit 1B Auxiliary Transformer Actuated,Resulting in Generator Trip & Reactor Trip.Caused by Electrical Fault. Loose Strand Removed from conductor.W/930511 Ltr ML20024G7191991-04-23023 April 1991 LER 91-001-00:on 910401,reactor Trip Occurred When Rod Dropped in Core.Caused by Defective Circuit Card in Rod Control Sys.Suspect Circuit Cards Replaced & Sent to Westinghouse for evaluation.W/910423 Ltr ML20043F1681990-06-0808 June 1990 LER 90-001-00:on 900512,reactor Tripped Due to lo-lo Water Level in Steam Generator 2A.Caused by Procedural Inadequacy. Procedure FNP-2-STP-151 Revised to Provide Addl Initial Conditions to Prevent Subj event.W/900608 Ltr ML20012D9591990-03-20020 March 1990 LER 90-002-00:on 900222,two Cases Found Where Surveillance Testing Procedures Did Not Perform All Tests Required by Tech Specs.Caused by Inadequate Procedural Guidance. Procedures revised.W/900320 Ltr ML20012C3031990-03-13013 March 1990 LER 90-001-00:on 900213,fire Watch Not Established within Required Time Period Due to Personnel Error.Administrative Procedure FNP-0-SOP-0.4 Revised & Personnel Retrained on requirements.W/900313 Ltr ML20012B4851990-03-0606 March 1990 LER 83-039/03X-2:on 830726,discovered That Handwheel for Inner Door of Personnel Airlock in Shut Position & Partially Opened.Caused by Excessive Use of Door During Outages.Door Repaired & Returned to Operable status.W/900306 Ltr ML19354E3341990-01-23023 January 1990 LER 89-016-00:on 891228,discovered That Required Surveillance for Plant Vent Stack Radioactive Gas Monitor Not Performed.Caused by Personnel Improperly Scheduling Surveillance for Time Later than Due date.W/900123 Ltr ML20011D5611989-12-18018 December 1989 LER 89-015-00:on 891118,reactor Tripped Due to Turbine Trip. Caused by Voltage Transient in Power Circuit to Digital electro-hydraulic Control Sys & Inverter Failure.Inverter Repaired & Returned to svc.W/891218 Ltr ML19332F9061989-12-13013 December 1989 LER 89-008-00:on 891113,containment Integrity Not Maintained for Approx 30 S.Caused by Personnel in That Inner Door Was Left Blocked Open.Personnel Counseled & Interim Administrative Controls established.W/891213 Ltr ML19332F6761989-12-12012 December 1989 LER 89-007-00:on 891112,both Motor Driven Auxiliary Feedwater Pumps Failed to Start Manually by Operator.Caused by Cognitive Personnel Error Re Design Change.Wiring Discrepancy Corrected & Pump Returned to svc.W/891212 Ltr ML19351A4571989-12-12012 December 1989 LER 89-014-00:from 891115-16,Tech Spec 3.0.3 Entered Voluntarily to Repair Leaking Containment Purge Isolation Dampers.Caused by Need to Repair Dampers.Dampers Closed & Automatic Isolation Feature restored.W/891212 Ltr ML19332F0851989-12-0707 December 1989 LER 89-006-00:on 891112,safety Injection & Reactor Trip Initiated Due to Low Steam Line Pressure.Caused by Personnel Error Involving Misconfiguration of Circuit Valve.Personnel Involved counseled.W/891207 Ltr ML19327C2621989-11-14014 November 1989 LER 89-012-00:on 891018,reactor Tripped Due to lo-lo Steam Generator Level Due to Closure of Governor Valves.Caused by Design Error in Digital electro-hydraulic Control Sys.Valve Position Limiter Feature removed.W/891114 Ltr ML19327C2671989-11-14014 November 1989 LER 89-013-00:on 891019,reactor Tripped Due to lo-lo Level in Steam Generator 2C.Caused by Operator Incorrectly Transferring Steam Generator Level Control to Main Feedwater.Involved Personnel counseled.W/891114 Ltr ML19354D4691989-11-0101 November 1989 LER 89-005-00:on 890930 & 1001,core Alterations Performed W/O Establishing Containment Refueling Integrity.Caused by Cognitive Personnel Error.Personnel Involved in Event Counseled.Containment Procedure strengthened.W/891101 Ltr ML19327B5451989-10-25025 October 1989 LER 89-011-00:on 890925,discovered That Tech Spec 4.6.3.1.a Surveillance Requirement Re Containment Air Lock Outer Door Not Done.Caused by Personnel Error.Individuals Involved Counseled Re Importance of Subj requirements.W/891025 Ltr ML19325D4941989-10-17017 October 1989 LER 89-004-00:on 890616,determined That Calculations Were Not Available to Demonstrate That Svc Water Sys Capable of Supplying Design Flow to safety-related Loads Under Scenario of Seismic event.W/891017 Ltr ML19325D2461989-10-12012 October 1989 LER 89-010-00:on 890920,reactor Tripped Manually Following Loss of Operating Steam Generator Feed Pump.Caused by Inadvertent Opening of Overspeed Trip Test Valve.Individual Involved in Event Counseled to Be More aware.W/891012 Ltr ML19325C7481989-10-10010 October 1989 LER 89-009-00:on 890525,determined That Power Range Nuclear Instrumentation Channels Reading Approx 7% Low.Equalizing Valves on Two of Three Instruments Were Leaking.Valves Repaired & Power Range Instruments adjusted.W/891010 Ltr ML20024F6841983-08-31031 August 1983 LER 83-031/03L-0:on 830806,during Testing,Instrumentation Channel Associated W/Level Transmitter LT-474 Declared Inoperable.Caused by Setpoint Drift of Comparator Card.Card Adjusted & Instrumentation Channel Declared Operable ML20024F6781983-08-31031 August 1983 LER 83-042/03L-0:on 830802,post-LOCA Hydrogen Recombiner 1A Declared Inoperable.Caused by Failure of Temp Indicator.New Indicator Installed & Declared Operable ML20024D0871983-07-26026 July 1983 LER 83-038/03L-0:on 830627,during Turbine Driven Auxiliary Feedwater Pump Inservice Test,Pump Failed to Start from Train a Steam Supply & Declared Inoperable.Caused by Valve HV-3226 Failing to Stroke properly.W/830726 Ltr ML20024C1251983-06-30030 June 1983 LER 83-027/03L-0:on 830607,during Performance of FNP-1-STP-43.0,train a Penetration Room Filtration Sys Declared Inoperable When Exhaust Fan Damper 3357A Would Not Open.Caused by Comparator Card failure.W/830630 Ltr ML20024C4011983-06-22022 June 1983 LER 83-025/03L-0:on 830528,during Calibr Procedure FNP-2-STP-612.0,reactor Coolant Pump 2A Undervoltage Relay 27-3 Declared Inoperable.Caused by Setpoint Drift.Relay Setpoint Adjusted ML20024C4061983-06-22022 June 1983 LER 83-024/03L-0:on 830525,following Increased Count Rate on Containment Atmosphere Particulate Monitoring Sys R-11, RCS Unidentified Leakage Found Above Tech Specs.Cause Not Stated.Loop B Drain Valve Tightened ML20023B5821983-04-29029 April 1983 LER 83-014/03L-0:on 830330,during Surveillance Test of Main Feedwater Pump Turbine 1A,RCS Tavg Decreased Below 541 F. Caused by Overfeeding of Steam Generators Due to Excessive Leak Past Main Feedwater Pump Discharge Valve ML20023B5281983-04-27027 April 1983 LER 83-015/03L-0:on 830328,instrumentation Channel Associated W/Steam Generator 1C Flow Transmitter FT-497 Declared Inoperable Due to Erroneous High Indication.Caused by Obstruction of Low Pressure Sensing Line.Line Cleared ML20023B5321983-04-27027 April 1983 LER 83-012/03L-0:on 830402,overtemp-delta Temp Loop 2 Channel II Declared Inoperable When Bistables 422C1-2 Tripped.Caused by Power Supply Failure of Comparator Card. Card Replaced & Loop Calibr ML20028G3051983-01-28028 January 1983 LER 82-062/03L-0:on 821231,noble Gas Activity Monitor R15 Declared Inoperable.Caused by Blown Fuse.Fuse Replaced & Monitor Returned to Svc ML20028G3111983-01-28028 January 1983 LER 83-001/03L-0:on 830102,RCS Subcooling Monitor Channel 2 Declared Inoperable Following Receipt of Main Control Board Alarms.Caused by Faulty Printed Circuit Card.Connector Pins on Card Cleaned ML20028G3091983-01-28028 January 1983 LER 82-063/03L-0:on 821230,B Train Chlorine Detector Declared Inoperable When Control Room Supply Damper Would Not Close.Caused by Faulty Solenoid Valve.Valve Replaced ML20027D9171982-11-0505 November 1982 LER 82-042/03L-0:on 821013,containment Auxiliary Personnel Hatch Failed to Meet Outer Door Acceptance Criteria.Caused by Worn Gaskets.Gaskets Replaced ML20027D3451982-10-26026 October 1982 LER 82-056/03L-0:on 820927,control Rod Bank D Declared Inoperable When Rods Would Not Move in Manual Control.Caused by Bank Select Relay Sticking,Causing Control Banks B & D to Be Selected Simultaneously.Relay Inspected & Reinstalled ML20027B7491982-09-21021 September 1982 LER 82-038/03L-0:on 820823,inboard & Outboard Pumps of Containment Atmosphere Monitors R-11 (Particulate Monitor) & R-12 (Gaseous Monitor) Declared Inoperable.Caused by Defective Relay & High Flow Switch.Relay & Switch Replaced ML20027B7471982-09-21021 September 1982 LER 82-036/03L-0:on 820824,2B Auxiliary Feedwater Pump Dc Control Power Breaker Inadvertently Opened.Caused by Personnel Error.Breaker Immediately Reclosed & Personnel Counseled ML20027B7461982-09-21021 September 1982 LER 82-051/03L-0:on 820823,1B Control Room Air Conditioner Failed,Rendering B Train Control Room Emergency Air Cleanup Sys Inoperable.Caused by Failed Fan Drive Belts.Belts Replaced & Sys Returned to Svc ML20027B7451982-09-21021 September 1982 LER 82-049/03L-0:on 820822,diesel Generator 1-2A Inadvertently Rendered Inoperable.Caused by Unauthorized Replacement of Lube Oil Strainers & Personnel Error. Generator Returned to Svc ML20052H6541982-04-30030 April 1982 LER 82-015/03L-0:on 820408,radiation Monitor 25A (Spent Fuel Storage Pool Area Gaseous activity-ventilation Sys Isolation) Declared Inoperable While Performing Test.Caused by Dirty Contacts on Mod Selector Switch.Contacts Cleaned ML20052H6591982-04-30030 April 1982 LER 82-017/03L-0:on 820413,FI-497 (Steam Generator 1C Feedwater Flow) Instrumentation Channel Declared Inoperable When Max Allowable Channel Check Error Was Exceeded.Caused by Faulty Transmitter Amplifier Card.Card Replaced ML20052C1391982-04-22022 April 1982 LER 82-014/03L-0:on 820326,28 & 0408,B Train Chlorine Detector Declared Inoperable Due to Detector Tape Not Advancing.Caused by Movement Indicator Binding Detector Tape & Sheared Pin in Tape Drive Mechanism ML20052C1371982-04-22022 April 1982 LER 82-014/03L-0:on 820328,while Performing Calibr & Functional Test,T average-low-low B Instrumentation Loop Declared Inoperable Due to Indicator Reading.Caused by Setpoint Drift.Power Supply Card Replaced ML20052C1401982-04-22022 April 1982 LER 82-015/03L-0:on 820325,radiation Monitor R29B Instrumentation Channel Declared Inoperable When Displays on All Readout Consoles Were Inaccurate.Caused by Dirty Contacts & Faulty Link.Contacts Cleaned ML20052C1351982-04-22022 April 1982 LER 82-012/03L-0:on 820326,during Routine Insp,Turbine Driven Auxiliary Feedwater Pump Declared Inoperable When Outboard Bearing Oil Bubbler Found Broken & Oil Drained. Possibly Caused by Workers Handling Scaffolding in Area ML20052A6571982-04-16016 April 1982 LER 82-013/03L-0:on 820317,containment Atmosphere Activity Monitors R-11 (Particulate Monitor) & R-12 (Gaseous Monitor) Declared Inoperable Due to Failure of Vacuum Pump.Caused by Failed Outboard Pump.Filter & Gasket Replaced ML20052A6671982-03-25025 March 1982 LER 82-009/03L-0:on 820228,instrumentation Loop Associated w/FT-474 (Steam Generator a Flow Transmitter) Declared Inoperable.Caused by Leaking Equalizing Valve.Valve Stem Repaired ML20052A6611982-03-25025 March 1982 LER 82-005/03L-0:on 820226,4160-volt B Train Ac Electrical Power Circuit Declared Inoperable When Emergency Bus 2G de-energized.Bus 2G de-energized When Breaker 2-DG15 Opened. Cause Under Investigation ML20052A6711982-03-25025 March 1982 LER 82-010/03L-0:on 820226,instrumentation Loop Associated w/LI-474 (Steam Generator a Level Indicator) Declared Inoperable.Caused by Loss of Necessary Level in Ref Leg While Steam Generator Not in Svc.Leg Refilled ML20052A6631982-03-25025 March 1982 LER 82-008/03L-0:on 820226,instrumentation Loop Associated w/LI-485 (Steam Generator B Level Indication) Declared Inoperable When Reading Was Out of Tolerance W/Other Channels.Caused by Obstruction in Ref Leg ML20050C1861982-03-19019 March 1982 LER 82-006/01T-0:on 820310,levels in Fire Protection Tanks a & B Fell to Approx 85,000 Gallons Each as Result of Inadvertent Actuation of Fire Protection Deluge Sys on Cooling Tower 1A.Caused by Personnel Error 1993-07-23
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217P0761999-10-0606 October 1999 Non-proprietary, Farley Units 1 & 2 LBB Calculation Results Due to SG Replacement & SG Snubber Elimination Programs ML20217G0361999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20212E7451999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Hcgs,Unit 1.With Summary of Changes,Tests & Experiments Implemented During Aug 1999.With ML20216E4941999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Jmfnp.With ML20210T2161999-08-0606 August 1999 Draft SE Supporting Proposed Conversion of Current TS to ITS for Plant ML20211B2011999-08-0404 August 1999 Informs Commission About Results of NRC Staff Review of Kaowool Fire Barriers at Farley Nuclear Plant,Units 1 & 2 & Staff Plans to Address Technical Issues with Kaowool & FP-60 Barriers ML20210R6031999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20196J3791999-06-30030 June 1999 Safety Evaluation of TR WCAP-14750, RCS Flow Verification Using Elbow Taps at Westinghouse 3-Loop Pwrs. Rept Acceptable ML20209G0661999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With L-99-267, Monthly Operating Repts for June 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With L-99-023, Monthly Operating Repts for May 1999 for Jfnp Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Jfnp Units 1 & 2. with ML20206G7471999-05-0404 May 1999 Safety Evaluation Accepting Corrective Actions Taken by SNC to Ensure That Valves Perform Intended Safety Functions & Concluding That SNC Adequately Addressed Requested Actions in GL 95-07 L-99-020, Monthly Operating Repts for Apr 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20206C9461999-04-30030 April 1999 1:Final Cycle 16 Freespan ODSCC Operational Assessment L-99-161, Monthly Operating Repts for Mar 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20205N0961999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20204D7271999-03-15015 March 1999 ISI Refueling 15,Interval 2,Period 3,Outage 3 for Jm Farley Nuclear Generating Plant,Unit 1 ML20207M6421999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20203A2651999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20199D8611999-01-12012 January 1999 SER Accepting Relief Request for Inservice Insp Program for Plant,Units 1 & 2 ML20199E6591998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20206C8081998-12-31031 December 1998 Alabama Power 1998 Annual Rept ML20198K4091998-12-18018 December 1998 COLR for Jm Farley,Unit 1 Cycle 16 ML20198B2561998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20195E2281998-11-16016 November 1998 Safety Evaluation Authorizing Relief Request for Second 10-year ISI Program Relief Request 56 for Plant,Unit 1 ML20195C9681998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20155E0271998-10-29029 October 1998 SER Approving & Denying in Part Inservice Testing Program Relief Requests for Plant.Relief Requests Q1P16-RR-V-3 & Q2P16-RR-V Denied Since Requests Do Not Meet Size Requirement of GL 89-04 ML20154B6121998-10-0101 October 1998 Safety Evaluation Granting Second 10-year ISI Requests for Relief RR-13 & RR-49 Through RR-55 for Jm Farley NPP Unit 1 ML20151V8341998-09-30030 September 1998 Non-proprietary Rev 2 to NSA-SSO-96-525, Jm Farley Nuclear Plant Safety Analysis IR Neutron Flux Reactor Trip Setpoint Change ML20154H6001998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20154H0121998-09-30030 September 1998 Submittal-Only Screening Review of Farley Nuclear Plant IPEEE (Seismic Portion) ML20197C8991998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Jm Farley Nuclear Plant,Units 1 & 2.With ML20237C5471998-08-20020 August 1998 Suppl to SE Re Amends 137 & 129 to Licenses NPF-2 & NPF-8, Respectively.Se Being Supplemented to Incorporate Clarifications/Changes & Revise Commitment for Insp of SG U-bends in Rows 1 & 2 for Unit 2 Only ML20236Y1121998-07-31031 July 1998 Voltage-Based Repair Criteria 90-Day Rept ML20237B1891998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Jm Farley Nuclear Plant,Units 1 & 2 ML20237A2181998-07-24024 July 1998 Jm Farley Unit 2 ISI Rept Interval 2,Period 3 Outage 1, Refueling Outage 12 ML20236U6141998-07-23023 July 1998 Safety Evaluation Authorizing Use of Alternative Alloy 690 Welds (Inco 52 & 152) as Substitute for Other Weld Metal ML20236R8671998-07-0909 July 1998 Safety Evaluation Concluding That Southern Nuclear Operating Co USI A-46 Implementation Program Has Met Purpose & Intent of Criteria in GIP-2 & Staff SSER-2 on GIP-2 for Resolution of USI A-46 ML20236M5981998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Jm Farley Nuclear Plant,Units 1 & 2 ML20154H0461998-06-30030 June 1998 Technical Evaluation Rept on Review of Farley Nuclear Plant IPEEE Submittal on High Winds,Flood & Other External Events (Hfo) ML20248M3121998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Jm Farley Nuclear Plant,Units 1 & 2 ML20247F3631998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Jm Farley Nuclear Plant,Units 1 & 2 ML20217D2591998-04-21021 April 1998 Safety Evaluation Accepting Licensee Proposed Alternative Re Augmented Exam of Reactor Vessel Shell Welds for Plant ML20247E8851998-03-31031 March 1998 FNP Unit 2 Cycle 13 Colr ML20217H3191998-03-31031 March 1998 Safety Evaluation Accepting Proposed Changes to Plant Matl Surveillance Programs ML20216D5941998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Joseph M Farley Nuclear Plant,Units 1 & 2 ML20217D4081998-03-24024 March 1998 Safety Evaluation Accepting Proposed Changes to Maintain Calibration Info Required by ANSI N45.2.4-1972 ML20216H6731998-03-17017 March 1998 SER Accepting Quality Assurance Program Description Change for Joseph M Farley Nuclear Plant,Units 1 & 2 ML20216J6851998-03-16016 March 1998 Revised Pages 58 & 59 to Fnp,Units 1 & 2,Power Uprate Project BOP Licensing Rept ML20216D9811998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Jm Farley Nuclear Plant,Units 1 & 2 1999-09-30
[Table view] |
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Alabama Power C:mpany '
'.1 40 inverness C;nter Parkwaj
,f .IJ - Post Office Box 1295-Birmingham. Alabame 35201 Telephono 205 868 5581. -l W. G. Hairston, til ' s Senior Vice President Nuclear Operations gghgg3 g the soutwn electrc system ,
v 10CFR50.73 L December 12, 1989 Docket No. 50-364
.U. S. Nuclear Regulatory Commission ATTN: Document Control Desk
-Washington, D.C. 20555 Dear Sir
~ Joseph M. Farley Nuclear Plant - Unit 2 Licensee Event Report No. LER 89-014-00 Joseph M. Farley Nuclear Plant, Unit 2 Licensee' Event Report No. LER 89-014-00 is being submitted in accordance with 10CFR50.73.
If you have any questions, please advise.
Respectfully submitted, l.
L l
.k.
. G. He.irston, III VGH,III/JARamd 8.60 l ' Enclosure l cci Mr. S. D. Ebneter
! Mr. G. F. Haxwell 1
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a FbnM 3es U.S. NUCLEMl u tiUL AT.4Y COeAMIS$10N d.PPROVED OMB tv0.31600"34 mire. 4 nom ;
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UCENSEE EYENT REPORT (LER) E'8u"E#Ti?"OA?DI'O ORD$N Es'TVJATl 8Al R(C%^R S AND REPORT $ MANAGEMENT ORANCH IP4301. U S NUCLE AR P APERWO K t i t'ON J ('3 60 O IC 06 MANAGEME NT AND SUDGET, WASHINGTON,DC 20603 FACILITY 8eaME (11 DOCKti NUMG4 R (2, PAGE (3) ]
Joseph M. Farley - Unit 2 o is l 0 l 0 1 o l 31 6l4 __1lorl 013 TITLt t4l Technical Specification 3.0.3 Entered To Repair Containment Purge Dampers IVENT DAf t ill L;R NueeBER tal REPORT DATE (M OTH&R f ACILITit4 INVOLVED (Si MONTH DAY YEAR YlAR 'Q '"L
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THIS REPORT 88 SUOMITTED PURdVANT TO THE RbOUtREMENTS OF 10 Cf R 6 (Cneca one or more of the tone.. net pu OPE RATINO 88004 m to 402thi l 20 40tlel to 734eH2Hal 73.7Hel R to.36teHil to.73teH2Hel 73.711el
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NAME TELEPHONE NUM0f R ARE A COQt D. N. Morey, General Manager-Nuclear Plant 2 05 N OOJ ti 1 'il 6 COMPLETE ONE LIN4 POR ( ACH COMPONEWT PAILURE DESCRitED IN THl3 REPORT (13)
CAUSE SYST E M COMPONtNT "h)$'g AC R O iA t '
o pn g CAU$6 SY STE M COMPONENT Mj C- R ' 4 O PR R Wl H nl Ml P l Dl j 11 1 (- V I I l l I l l I I I I I I I I I I I I I I SUPPLthalNT AL REPORT E kPECTED I141 MONTH DAY YEAR
$V8M153 ION i Yt$ (It ven cornotete 4xPLCTtO $Ugeets;isON OA Til NO l l l AesmCT a,-,, w un soeceu e . mn. ee ureenno,e are on,n.,, s so oes Over the period of time from 1443 on 11-15-89 to 1411 on 11-16-89, Technical Specification 3.0.3 vas entered voluntarily a total of six times for short periods of time in order to repair leaking containment purge isolation dampers.
Technical Specification 3.0.3 vas in effect because the automatic isclation capability of a containment purge damper had been deactivated and the damper was subsequently opened in order to effect the repair of the leaking containment purge dampers. Technical Specification 3.0.3 was in effect for a total of 38 minutes during the two days.
The dampers were closed immediately after each opening. The automatic isolation feature which had been made inoperable to allow repairs was restored after repairs were completed. The containment purge dampers vill be tested for leakage at an increased frequency until as-found leakage rates between tests remain relatively c.onstant.
EC f orm 366 4: 491
N U.S. iUCLE%t ReiULATORY COMhNaB@N
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- i. PPT.OVED oms NO. 31604104 1 K?l7.88. 4/30CJ UCENSEE EVENT REPORT (LER) (5ls*tTAio",u"8We',foa8!!?vilt%0MY
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r TEXT CONTINUATION cg4",7#,S^L" M MEN!MUin,'h'n".'"En 1 PAPE RWO R TION t'3 60 04 BC 07 MANAGEMENT AND $UDGET,W ASHINGTON, DC 20603.
FACILITY NAME til DOCKET NUM0ER (2) LER NUMetR (Si PAGE 13)
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Plant and System Identification Westinghouse - Pressurized Vater Reactor Energy Industry Identification System codes are identified in the text as [XX].
Summary of Event f Over the period of time from 1443 on 11-15-89 to 1411 on 11-16-89, Technical i Specification 3.0.3 was entered voluntarily a total of six times for short periods of time in order to repair leaking containment purge isolation dampers [NH].
Technical Specification 3.0.3 was in effect because the automatic isolation capability of a containment purge damper had been deactivated and the damper was subsequently opened in order to effect the repair of the leaking containment purge dampers. Technical Specification 3.0.3 was in effect for a total of 38 minutes during the two days. ,
Description of Event On 11-15-89, the unit was operating at approximately 100 percent power and testing ,
of.the containment purge supply isolation dampers was being conducted per L FNP-2-STP-627.2 (Leak Testing of The Containment Purge System). Each containment purge line has two dampers in series. Testing is done by pressurizing between the dampers.
At 0904, the containment purge supply isolation dampers were found to have leakage i rates that could potentially be in excess of Technical Specification limits. The action statement for Technical Specification 3.6.1.7 requires that within twelve I hours the-leakage be reduced within limits or the penetration isolated on at least one side of the containment boundary.
Repair of the containment purge supply isolation dampers required opening the 48-inch damper outside containment (02P13V281) to allow personnel access for damper adjustments. Personnel safety concerns required deactivation of this damper's l
l automatic isolation function. The dt.mper inside containment remained closed with its automatic isolation capability operable throughout this event.
In order to eliminate the excessive leakage as soon as possible, it was decided to make the required adjustments to the damper seats at current plant conditions rather than vait for the plant to be placed in a condition where the automatic actuation logic for purge and exhaust isolation was not required (Mode 5 - Cold Shutdown). It would have required 15-20 hours to place the unit in Mode 5.
With the automatic isolation capability of 02P13V281 deactivated, Technical Specification 3.3.2 was entered. Action Statement 17 associated with Table 3.3-3 of Technical Specification 3.3.2 requires that the inoperable containment purge damper (s) be maintained closed. During the time the damper was opened to allow access for repairs, the action statement for Technical Specification 3.3.2 was not met and Technical Specification 3.0.3 was entered.
,'RC Poem 308A (649) i
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(MPIRES 4/30/92
, LICENSEE EVENT REPORT (LER) fy'ls'Ol & *d R d',"J 5,io"n ,' %cgig ,v y<,tgtyg N TEXT CONTINUATION CJ",'t,'o',"4 M^" !"oWf',Mc','#,'M ',".' "Mf!
1 PAPERWD RE b i TON J 604 1 OF MANAGEME NT AND BuDOt),W ASHINGTON, DC 20603.
FACILITY hAML (Il pocett Y NUMSEM (21 ggg gygggg ggi pagg g33
- ua "==. O'#,'N Farley Nuclear Plant - Unit 2 o ls ;o jo jo l 3l q 4 8;9 0,1l 4 J ;0 0 [3 or ftXT W snese ausse 4 tovuseel use ashamsvia/ M,C Fame ms (th 0 l3 02P13V281 was opened and Technical Specification 3.0.3 was entered voluntarily four separate times on 11-15-89 for a total of 22 minutes. The longest period Technical Specification 3.0.3 was in effect at any one time was 11 minutes.
These periods were 1443 - 1454, 1502 - 1505, 1628 - 1633, and 1646 - 1649.
Leakage testing performed subsequent to adjustment of 02P13V281 proved that the actual leakage through any purge supply isolation damper was not in excess of the Technical Specification 3.6.1.7 limits.
The containment purge exhaust dampers were tested on 11-16-89. Although the ceasured leakage was less than the Technical Specification limit, it was considerably higher than the leakage measured during the previous test which was performed three months earlier. A decision was made to reduce the leakage even though the Technical Specification limit was not exceeded. The exhaust dampers were adjusted during operation in a manner similar to the supply dampers. Technical Specification 3.0.3 was in effect twice for a total of 16 minutes on 11-16-89. The periods were 1340 - 1351 and 1406 - 1411.
Cause of Event Technical Specification 3.0.3 was entered voluntarily to allow access to the damper seats so that the leaking containment purge dampers could be repaired.
Reportability Analysis and Safety Assessment The event is reportable because Technical Specification 3.0.3 was entered. However,
'lechnical Specification 3.0.3 was in effeet for no more than eleven minutes at a time end for a-total of only 38 minutes over a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period. The Technical Specification 3.6.1.7 nction statement requirements for the purge supply and exhaust dampers were met at all times. One of the two dampers in each line remained closed with its automatic isolation capability operable throughout the event. No adverse condition resulted and there was no effect on plant operation. The health and safety of the public vere not affected by this event.
Corrective Action The dampers were closed immediately after each opening. The automatic l isolation feature which had been made inoperable to allow repairs was restored l- ofter repairs were completed. The containment purge dampers vill be tested l for leakage at an increased frequency until as-found leakage rates between L tests remain relatively constant.
1 Additional Information No similar LER'S have been submitted by FNP.
The dampers are NR1A containment purge isolation dampers made by Henry Pratt Co.
This event would not have been more severe if it had occurred under different operating conditions.
E'MC Form 355A (689)