05000348/LER-1979-027-03, /03L-0 on 790607:radiation Monitor Declared Inoperable.Caused by Pump Malfunction.Pump Repaired & Declared Operable 790615

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/03L-0 on 790607:radiation Monitor Declared Inoperable.Caused by Pump Malfunction.Pump Repaired & Declared Operable 790615
ML19225B262
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 07/19/1979
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19225B252 List:
References
LER-79-027-03L, LER-79-27-3L, NUDOCS 7907240379
Download: ML19225B262 (1)


LER-1979-027, /03L-0 on 790607:radiation Monitor Declared Inoperable.Caused by Pump Malfunction.Pump Repaired & Declared Operable 790615
Event date:
Report date:
3481979027R03 - NRC Website

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r L 74 n-HaouTuAIE m3 t\\ L".T D~0CIUP16CN Ar;c nic 'AULE CONStout% Cts h E.>J [ At 1020 on 6/7/79, radiation monitor R25A (Fue1 Sterace Pool Area. Gaseous Activity - l p -'O Lvent11ation system Isolation) was declared inoperable due to pump failure. Tech. Specj [njg l section 3.3.'..I and table 3.3.6 require.s a minimum of two radiation menitor channels o 1. I I to be cperable for the fuel storage area.

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