05000348/LER-1979-024-03, /03L-0 on 790622:during Review of Surveillance Tests FNP-1-STP-40.1 & 40.2,noted That Certain Components Were Not Included in Test Procedures.Caused by Procedural Deficiencies.Procedure Change Has Been Made

From kanterella
(Redirected from ML19225B261)
Jump to navigation Jump to search
/03L-0 on 790622:during Review of Surveillance Tests FNP-1-STP-40.1 & 40.2,noted That Certain Components Were Not Included in Test Procedures.Caused by Procedural Deficiencies.Procedure Change Has Been Made
ML19225B261
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 07/19/1979
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19225B252 List:
References
LER-79-024-03L, LER-79-24-3L, NUDOCS 7907240376
Download: ML19225B261 (1)


LER-1979-024, /03L-0 on 790622:during Review of Surveillance Tests FNP-1-STP-40.1 & 40.2,noted That Certain Components Were Not Included in Test Procedures.Caused by Procedural Deficiencies.Procedure Change Has Been Made
Event date:
Report date:
3481979024R03 - NRC Website

text

'"?

UCENSEE EVEN T REPORT

^

pL..LJ l

l_l@

wor ^st enmi on im e.tt ntouinco monr.muw co.w et occ kJi] la I r. I d i n i r LLJ@l 0101-1010101O!0 -l 01 O l@l 4111 1 I il ll@l l

l sicAr.,3@

4 a o.c<t.

.a i:

a imrr.. w iin x

Lictrn.c ivrt si

- u.~. n l,}],5

.V 2.! l L M0_l 5 l 0 l 0 l0 1314 l8 l@l 0 l 6 l 2 l 2 7 l 9_j@l 0 ] 7 l 1 l 9 l 7 l 9 l@

S,c.$.'m,c a.$$.$m $

~~ ^

.~,

t.,

{T--] l At 1100 on 6/22/79 during a review of : surveillance tests FNP-1-STP-40.1 and 40.2 l

[7-l-q [ (Sequencer load shedding tests), it was determined that certain components (battery l

g.:j { charger IC: service water pump 1C; load centers la, IC, IF; bus tie between F and 11; ;

FTT] i bus tie between G an ' J ', acre not included in these STP's.

Tech. Spec. 4.8.1.1.2.c.3.3

_ _J y,_j l requires verification of load shedding from the erergenc', buses'at l' east once per 18 g O

7 l Inontiis during shutdesn.

The above cor.ponents sere checked during the performance of g Unit 1 pre-op testing (early 1977).

The health and safety of the public were not g

gg l 6J 7

8 9 affected by this event.

SYSTEV CA.;E CAU 5 C o'.' a.

VALVE CCCf CoCE 5_=^r's CO.'70* E '. T CCO:

SURCODE

. SUE; COD E o

9 i el El@ lnl@ Iz l@

zl zi zi zi zl zlO [z J@ Iz l@

7 8

9 10 il 12 13 10 19_

23 SE Ou!'.TIAL CCCUnnENCE RE7097 fiEVISION t c t-r3 V E *. T Y E A H RE 5enT NO CCDE TYFC No.

O f '::;[L 719) l-l l0 l2 I4 l

\\/l

[ 7l 3 l lL l l-l l0l 21 2

^;

g 27

/3

')

30 3.

32 A T:C '. FLTUaf Er> _;,

$% _ t 7.

ATT Ai h*.-NT ri?AD 3 PDi".1E COYo.

Co'.5 ?O N E N T SU3 vet T ED F OR'.1 du a.

SUPP Lt E n MANUF ACTUaEa T Ar.E 5 F4 7. C'.

O'.PLI I'd NCUR5 4'

I@

l 0 10 l 0 l 0 l [N_J @

W@

l zl@

l z l 9 l 9 l 9 '/]

I Clh,\\' l@

lz!{

7

,e' 40 41 42 43 44 4;

J,.

,J+

  • s

...y.s @

c A H c:5:wTioN a. ; cce=r:n was caused by procedural deficiencies.

Apparently, when the STP's were [This event i

o l written, sequencer drawings,cere used to determine the loads which are shed, rather l

i i

; jthan usinr the load sned draeings.

A procedure change has beca made to correct the 3

lSTP omissions.

Alv, the revised surveillance tests will be performed prior to the y

l plant entering nede 4.

7 41 5 60 r.'i. T" On C F 9 :.a 1

m, S i i. i t,

  • r O /. ' '

OTHi a sis rus -

Dr.,;C// L ei f DISCOVERY DESCnirTION 3 0 l 0 l 0 ll[ ! '

l l B l@l Review of Surveill.ance Test Procedures l

1

~.

7 F.

'1 p.

1 44 4a 46 E0 (Li t.L.

,s,.IQr AZ il% :T v

'OC ATIO*J OF RELE A;C u

l I

N^

I L,LL'd LzJ @ L2J3l m

u c

fi' r.Q L ( > Do ;ps t

Lu,.J 101 OI OJOf

_.mo zu NA i

mn Ml,h h I

1010 J

l

)gwp e

g

.g l_b [z[ ll NA

.y,,

l JOU lfI7 u

fd 7907240 3 76

- nuc uu wn v I-.!,.'l'LL

"' s

.~

i NA l

IIIIIIIILLLU LG G3 b

W.

G.

Ila i rs t on, III (205) 899-5156 n

Fv