ML18139A987: Difference between revisions

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See also: [[followed by::IR 05000280/1980039]]


=Text=
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{{#Wiki_filter:' * .. *.~ .. ;:~ ~-:. t r. * ** ;.1,1 -.* -VIRGINIA ELECTRIC AND POWER. COMPANY RICHMOND,VIRGIN.IA  
{{#Wiki_filter:' * .. *.~ .. ;:~ ~-:. t r. * ** ;.1,1 -.* -VIRGINIA ELECTRIC AND POWER. COMPANY RICHMOND,VIRGIN.IA 23261
23261 * r.: " Io . . J i.1 :_ ._. * '-: December 17, 1980 \: .. .... 00 Serial No. 971 NO/RMT:ms  
* r.: " Io . . J i.1 :_ ._. * '-: December 17, 1980 \: .. .... 00 Serial No. 971 NO/RMT:ms Mr. James P. O'Reilly, Director Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, Suite 3100 Atlanta, Georgia 30303 Docket Nos. 50-280 50-281 License Nos. DPR-32 DPR-37  
Mr. James P. O'Reilly, Director Office of Inspection  
 
and Enforcement  
==Dear Mr. O'Reilly:==
U. S. Nuclear Regulatory  
 
Commission  
We have reviewed your letter of November 25, 1980 in reference to the inspection conducted at Surry Power Station on September 2 through October 3, 1980 and reported in IE Inspection Report Nos. 50-280/80-39 and 50-281/80-43.
Region II 101 Marietta Street, Suite 3100 Atlanta, Georgia 30303 Docket Nos. 50-280 50-281 License Nos. DPR-32 DPR-37 Dear Mr. O'Reilly:  
Our responses to the specific infractions are attached.
We have reviewed your letter of November 25, 1980 in reference  
We determined that no proprietary information is contained reports. Accordingly, the Virginia Electric and Power Company objection to these inspection reports being made a matter of disclosure.
to the inspection  
have Attachment cc: Mr. Steven A. Varga, Chief Operating Reactors Branch No. 1 Division of Licensing Very truly yours, ./,1 ,.!* '\/ / >;t .. ; /;i: .. B. R. Sylvia Manager -Nuclear Operations and Maintenance in the has no public   
conducted  
* *
at Surry Power Station on September  
* SURRY POWER STATION RESPONSE TO NOTICE OF VIOLATION REPORTED IN APPENDIX A OF IE REPORT 50-280/80-39 AND 50-281/80-43 Attachment Page 1 NRC COMMENTS:
2 through October 3, 1980 and reported in IE Inspection  
A. As required by 10 CFR 50.59 and Section 14 of the VEPCO NPS QA Manual, the licensee may make changes to the facility as described in the FSAR, provided that records of these changes are maintained and include a written safety evaluation which determined that the change does not involve an unreviewed safety question.
Report Nos. 50-280/80-39  
In addition, Section 14 of the QA Manual requires the maintenance of the Jumper Log Book and forms, listing the status of each installed jumper or temporary modification for jumpers not installed by an approved procedure.
and 50-281/80-43.  
Contrary to the above, on September 12, 1980 the inspector observed that the Unit 2 Safeguards Valve Pit Sump piping had been modified by the installation of jumper hose on the piping valve 2-DA-43, and no record, safety evaluation, procedure, or jumper log entry for the installation has been completed.
Our responses  
The jumper, with 2-DA-43 open, apparently led to the inadvertent diversion of Unit 1 and 2 containment sump water into the Unit 2 Safeguards Building Valve Pit (basement), where several feet of radioactive standing water was observed.
to the specific infractions  
This is an infraction and applies to Unit 2. RESPONSE:
are attached.  
The item is correct as stated. The jumper discussed above is a hose from the discharge of a temporary sump pump. This was installed due to failures of both installed sump pumps. All water transfers were within the enclosed building.
We determined  
A jumper had been issued and implemented in January of 1980 to accomplish the job of pumping the valve pit. A new temporary pump was installed in September; however, the jumper log was not amended. During reviews of the log it was assumed the jumper was installed as originally approved.
that no proprietary  
: 1. 2. 3. Corrective steps which have been taken and the results achieved:
information  
The out of date jumper lQg was terminated and a new jumper log was issued to reflect the existing conditions.
is contained  
The discharge hose was moved to a floor drain which directs water to the Liquid Waste System. The standing water was pumped and processed.
reports. Accordingly, the Virginia Electric and Power Company objection  
Maintenance has been completed on the installed pumps and the system returned to its proper configuration.
to these inspection  
Corrective steps which will be taken to avoid further non-compliance:
reports being made a matter of disclosure.  
Operational personnel were instructed as to the requirements of jumpers . This includes proper notification, logging, and documentation.
have Attachment  
The date when full compliance will be achieved:
cc: Mr. Steven A. Varga, Chief Operating  
Full compliance has been achieved.
Reactors Branch No. 1 Division of Licensing  
NRC COMMENT: Attachment Page 2 B. As required by Technical Specification 3.10.A.l, the containment ment door (hatch) shall be properly closed during refueling conditions.
Very truly yours, ./,1 ,.!* '\/ / >;t .. ; /;i: .. B. R. Sylvia Manager -Nuclear Operations  
Contrary to the above, on September 24, 1980 the inspector observed that the Unit 1 containment escape hatch was not installed in the equipment door and the blank metal flange installed on the equipment door to substitute for the escape hatch was not properly sealed during refueling operations.
and Maintenance  
This is an infraction and applies to Unit 1. RESPONSE:
in the has no public   
This is correct as stated. The intent of containment integrity is to lish a gas-tight envelope during fuel movement operations.
* * * SURRY POWER STATION RESPONSE TO NOTICE OF VIOLATION  
The containment was in a sub-atmospheric condition at all times with only exhaust ventilation equipment in operation.
REPORTED IN APPENDIX A OF IE REPORT 50-280/80-39  
: 1. Corrective steps which have been taken and the results achieved:
AND 50-281/80-43  
When the situation was identified, refueling was stopped until the door was sealed temporarily to establish a gas-tight seal. 2. Corrective steps which will be taken to avoid further non-compliance:
Attachment  
A more permanent sealing was installed during a period when no fuel movement was in progress.
Page 1 NRC COMMENTS:  
The refueling procedure has been revised to insure this hatch is properly sealed prior to fuel movement.
A. As required by 10 CFR 50.59 and Section 14 of the VEPCO NPS QA Manual, the licensee may make changes to the facility as described  
: 3. The date when full compliance will be achieved:
in the FSAR, provided that records of these changes are maintained  
Full compliance has been achieved.}}
and include a written safety evaluation  
which determined  
that the change does not involve an unreviewed  
safety question.  
In addition, Section 14 of the QA Manual requires the maintenance  
of the Jumper Log Book and forms, listing the status of each installed  
jumper or temporary  
modification  
for jumpers not installed  
by an approved procedure.  
Contrary to the above, on September  
12, 1980 the inspector  
observed that the Unit 2 Safeguards  
Valve Pit Sump piping had been modified by the installation  
of jumper hose on the piping valve 2-DA-43, and no record, safety evaluation, procedure, or jumper log entry for the installation  
has been completed.  
The jumper, with 2-DA-43 open, apparently  
led to the inadvertent  
diversion  
of Unit 1 and 2 containment  
sump water into the Unit 2 Safeguards  
Building Valve Pit (basement), where several feet of radioactive  
standing water was observed.  
This is an infraction  
and applies to Unit 2. RESPONSE:  
The item is correct as stated. The jumper discussed  
above is a hose from the discharge  
of a temporary  
sump pump. This was installed  
due to failures of both installed  
sump pumps. All water transfers  
were within the enclosed building.  
A jumper had been issued and implemented  
in January of 1980 to accomplish  
the job of pumping the valve pit. A new temporary  
pump was installed  
in September;  
however, the jumper log was not amended. During reviews of the log it was assumed the jumper was installed  
as originally  
approved.  
1. 2. 3. Corrective  
steps which have been taken and the results achieved:  
The out of date jumper lQg was terminated  
and a new jumper log was issued to reflect the existing conditions.  
The discharge  
hose was moved to a floor drain which directs water to the Liquid Waste System. The standing water was pumped and processed.  
Maintenance  
has been completed  
on the installed  
pumps and the system returned to its proper configuration.  
Corrective  
steps which will be taken to avoid further non-compliance:  
Operational  
personnel  
were instructed  
as to the requirements  
of jumpers . This includes proper notification, logging, and documentation.  
The date when full compliance  
will be achieved:  
Full compliance  
has been achieved.
NRC COMMENT: Attachment  
Page 2 B. As required by Technical  
Specification  
3.10.A.l, the containment ment door (hatch) shall be properly closed during refueling  
conditions.  
Contrary to the above, on September  
24, 1980 the inspector  
observed that the Unit 1 containment  
escape hatch was not installed  
in the equipment  
door and the blank metal flange installed  
on the equipment  
door to substitute  
for the escape hatch was not properly sealed during refueling  
operations.  
This is an infraction  
and applies to Unit 1. RESPONSE:  
This is correct as stated. The intent of containment  
integrity  
is to lish a gas-tight  
envelope during fuel movement operations.  
The containment  
was in a sub-atmospheric  
condition  
at all times with only exhaust ventilation  
equipment  
in operation.  
1. Corrective  
steps which have been taken and the results achieved:  
When the situation  
was identified, refueling  
was stopped until the door was sealed temporarily  
to establish  
a gas-tight  
seal. 2. Corrective  
steps which will be taken to avoid further non-compliance:  
A more permanent  
sealing was installed  
during a period when no fuel movement was in progress.  
The refueling  
procedure  
has been revised to insure this hatch is properly sealed prior to fuel movement.  
3. The date when full compliance  
will be achieved:  
Full compliance  
has been achieved.
}}

Revision as of 17:15, 31 July 2019

Responds to NRC 801125 Ltr Re Violations Noted in IE Insp Repts 50-280/80-39 & 50-281/80-43.Corrective Actions:Maint Completed on Installed Pumps & Refueling Procedure Revised
ML18139A987
Person / Time
Site: Surry  Dominion icon.png
Issue date: 12/17/1980
From: Sylvia B
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18139A986 List:
References
971, NUDOCS 8101160696
Download: ML18139A987 (3)


Text

' * .. *.~ .. ;:~ ~-:. t r. * ** ;.1,1 -.* -VIRGINIA ELECTRIC AND POWER. COMPANY RICHMOND,VIRGIN.IA 23261

  • r.: " Io . . J i.1 :_ ._. * '-: December 17, 1980 \: .. .... 00 Serial No. 971 NO/RMT:ms Mr. James P. O'Reilly, Director Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, Suite 3100 Atlanta, Georgia 30303 Docket Nos. 50-280 50-281 License Nos. DPR-32 DPR-37

Dear Mr. O'Reilly:

We have reviewed your letter of November 25, 1980 in reference to the inspection conducted at Surry Power Station on September 2 through October 3, 1980 and reported in IE Inspection Report Nos. 50-280/80-39 and 50-281/80-43.

Our responses to the specific infractions are attached.

We determined that no proprietary information is contained reports. Accordingly, the Virginia Electric and Power Company objection to these inspection reports being made a matter of disclosure.

have Attachment cc: Mr. Steven A. Varga, Chief Operating Reactors Branch No. 1 Division of Licensing Very truly yours, ./,1 ,.!* '\/ / >;t .. ; /;i: .. B. R. Sylvia Manager -Nuclear Operations and Maintenance in the has no public

  • *
  • SURRY POWER STATION RESPONSE TO NOTICE OF VIOLATION REPORTED IN APPENDIX A OF IE REPORT 50-280/80-39 AND 50-281/80-43 Attachment Page 1 NRC COMMENTS:

A. As required by 10 CFR 50.59 and Section 14 of the VEPCO NPS QA Manual, the licensee may make changes to the facility as described in the FSAR, provided that records of these changes are maintained and include a written safety evaluation which determined that the change does not involve an unreviewed safety question.

In addition, Section 14 of the QA Manual requires the maintenance of the Jumper Log Book and forms, listing the status of each installed jumper or temporary modification for jumpers not installed by an approved procedure.

Contrary to the above, on September 12, 1980 the inspector observed that the Unit 2 Safeguards Valve Pit Sump piping had been modified by the installation of jumper hose on the piping valve 2-DA-43, and no record, safety evaluation, procedure, or jumper log entry for the installation has been completed.

The jumper, with 2-DA-43 open, apparently led to the inadvertent diversion of Unit 1 and 2 containment sump water into the Unit 2 Safeguards Building Valve Pit (basement), where several feet of radioactive standing water was observed.

This is an infraction and applies to Unit 2. RESPONSE:

The item is correct as stated. The jumper discussed above is a hose from the discharge of a temporary sump pump. This was installed due to failures of both installed sump pumps. All water transfers were within the enclosed building.

A jumper had been issued and implemented in January of 1980 to accomplish the job of pumping the valve pit. A new temporary pump was installed in September; however, the jumper log was not amended. During reviews of the log it was assumed the jumper was installed as originally approved.

1. 2. 3. Corrective steps which have been taken and the results achieved:

The out of date jumper lQg was terminated and a new jumper log was issued to reflect the existing conditions.

The discharge hose was moved to a floor drain which directs water to the Liquid Waste System. The standing water was pumped and processed.

Maintenance has been completed on the installed pumps and the system returned to its proper configuration.

Corrective steps which will be taken to avoid further non-compliance:

Operational personnel were instructed as to the requirements of jumpers . This includes proper notification, logging, and documentation.

The date when full compliance will be achieved:

Full compliance has been achieved.

NRC COMMENT: Attachment Page 2 B. As required by Technical Specification 3.10.A.l, the containment ment door (hatch) shall be properly closed during refueling conditions.

Contrary to the above, on September 24, 1980 the inspector observed that the Unit 1 containment escape hatch was not installed in the equipment door and the blank metal flange installed on the equipment door to substitute for the escape hatch was not properly sealed during refueling operations.

This is an infraction and applies to Unit 1. RESPONSE:

This is correct as stated. The intent of containment integrity is to lish a gas-tight envelope during fuel movement operations.

The containment was in a sub-atmospheric condition at all times with only exhaust ventilation equipment in operation.

1. Corrective steps which have been taken and the results achieved:

When the situation was identified, refueling was stopped until the door was sealed temporarily to establish a gas-tight seal. 2. Corrective steps which will be taken to avoid further non-compliance:

A more permanent sealing was installed during a period when no fuel movement was in progress.

The refueling procedure has been revised to insure this hatch is properly sealed prior to fuel movement.

3. The date when full compliance will be achieved:

Full compliance has been achieved.