ML20136F538: Difference between revisions

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{{#Wiki_filter:i.
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                      ,                                                                                ?? Y' APPENDIX A-                                        '-
r                      7                ,
NOTICE OF VIOLATION                                        3
                                                ' Kansas Gas'and Electric Company                                              -
Docket: 50-482/85  p                                              _W olf Creek Generating Station ~                                                                          License: ' NPF-421
                                                                      =-
: a.                                          ,
                                                "During an NRCfinspection . conducted during -Octpber 1985,- a violatio'niof- NRC                                                                                            ,
e s      .
requirements ' was . identified. The violation involved the failure to isolate a
                                          ,      nonseismic' sight glass ~ level gage. In accordance with the " General Statement.of Policy.and. Procedure for:NRC Enforcement Actions,"
                                                ,10 CFRrPart 2, Appendix'C (1985), the. violation is listed below:
J'                                                          - Nonseismic Sight Glass Level Gage N'ot Isolated s      ,,
r        <10 CFR-Part 50, Appendix.B,; Criterion V states','in part, " Activities
                                                              . affecting quality.,shall be prescribed by documented ~ instructions,
: y.                    .,
Lprocedures, or. drawings = of a type appropriate to the circumstances. . . ."
The Checklist (CKL) EG-120, Revision 5, " Component Cooling Water System -
Valv'e, Switch, and Breaker Lineup,!' has been established in accordance with 10 CFR Part 50; Appendix B, Criterion V.
              ~                          '
l Contrary to the above, CKL EG-120 was inappropriate to the circumstances in.that Valves EG-V 160, 161, 171, and 172 were opened in accordance twith Checklist A of CKL EG-120 when the valves should have been closed
                                                              .due to the'1evel gage between-the valves being nonseismic.
                                                          +
This is"a Severity Level-IV violation.(Suppleme.nt I.D).(50-482/8537-01).
                                                .Pursua'n t to the provisions of 10 CFR 2.201,~ Kansas Gas and Electric Company is.hereby required to submit to this'0ffice, within 30 days of the date of
                                                -the >1etter transmitting this Notice, a written statement- or explanation in reply, including: (1) the reason for-the violation'if admitted, (2) the
                                                . corrective steps which have been taken and the results achieved; (3). the corrective. steps which will be taken to avoid further violations; and-                                                                                                      '
: h.                                            '(4) thefdate when full ~ compliance will be' achieved. ,Where good cause.is                                                                                                  ,
shown, consideration will be given to extending the response time.
e Dated at Arlington,: Texas '                                                                                                                                                .
        'k -                                      this Ja/ day of 4 //e m  -
1986.
u                                                                                f, t
                                                                                                    =
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POR              ADOCK O PDR G                                  ,,                                                          ;
7                '            '
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                                                                                          ,            -7,,n                                      -    en      - , +      n 4 . p..-.                ,,    ~w-}}

Latest revision as of 03:28, 1 July 2020

Notice of Violation from Insp on 851005-1130
ML20136F538
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 01/02/1986
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20136F533 List:
References
50-482-85-37, NUDOCS 8601070423
Download: ML20136F538 (1)


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,  ?? Y' APPENDIX A- '-

r 7 ,

NOTICE OF VIOLATION 3

' Kansas Gas'and Electric Company -

Docket: 50-482/85 p _W olf Creek Generating Station ~ License: ' NPF-421

=-

a. ,

"During an NRCfinspection . conducted during -Octpber 1985,- a violatio'niof- NRC ,

e s .

requirements ' was . identified. The violation involved the failure to isolate a

, nonseismic' sight glass ~ level gage. In accordance with the " General Statement.of Policy.and. Procedure for:NRC Enforcement Actions,"

,10 CFRrPart 2, Appendix'C (1985), the. violation is listed below:

J' - Nonseismic Sight Glass Level Gage N'ot Isolated s ,,

r <10 CFR-Part 50, Appendix.B,; Criterion V states','in part, " Activities

. affecting quality.,shall be prescribed by documented ~ instructions,

y. .,

Lprocedures, or. drawings = of a type appropriate to the circumstances. . . ."

The Checklist (CKL) EG-120, Revision 5, " Component Cooling Water System -

Valv'e, Switch, and Breaker Lineup,!' has been established in accordance with 10 CFR Part 50; Appendix B, Criterion V.

~ '

l Contrary to the above, CKL EG-120 was inappropriate to the circumstances in.that Valves EG-V 160, 161, 171, and 172 were opened in accordance twith Checklist A of CKL EG-120 when the valves should have been closed

.due to the'1evel gage between-the valves being nonseismic.

+

This is"a Severity Level-IV violation.(Suppleme.nt I.D).(50-482/8537-01).

.Pursua'n t to the provisions of 10 CFR 2.201,~ Kansas Gas and Electric Company is.hereby required to submit to this'0ffice, within 30 days of the date of

-the >1etter transmitting this Notice, a written statement- or explanation in reply, including: (1) the reason for-the violation'if admitted, (2) the

. corrective steps which have been taken and the results achieved; (3). the corrective. steps which will be taken to avoid further violations; and- '

h. '(4) thefdate when full ~ compliance will be' achieved. ,Where good cause.is ,

shown, consideration will be given to extending the response time.

e Dated at Arlington,: Texas ' .

'k - this Ja/ day of 4 //e m -

1986.

u f, t

=

j82 8601070423'86 -

POR ADOCK O PDR G ,,  ;

7 ' '

- .u. .

s mn -y c. , , , -x n,-- , - --

, -7,,n - en - , + n 4 . p..-. ,, ~w-