ML20216A905

From kanterella
Jump to navigation Jump to search
Insp Rept 50-482/98-10 on 980308-0418.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML20216A905
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 05/06/1998
From: Johnson W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20216A877 List:
References
50-482-98-10, NUDOCS 9805140295
Download: ML20216A905 (27)


See also: IR 05000482/1998010

Text

.

%

'

ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket No.: 50-482

License No.: NPF-42

Report No.: 50-482/98-10-

Licensee: Wolf Creek Nuclear Operating Corporation

<

Facility: Wolf Creek Generating Station

Location: 1550 Oxen Lane, NE

Burlington, Kansas

Dates: March 8 through April 18,1998

Inspectors: J. F. Ringwald, Senior Resident inspector

B. A. Smalldridge, Resident inspector

R. V. Azua, Project Engineer

K. M. Thomas, Project Manager, Office of Nuclear Reactor Regulation

Approved: W. D. Johnson, Chief, Project Branch B

ATTACHMENT: Supplemental Information

l

l

!

)

1

l

l

i

i

l

9805140295 990506 2

DR ADOCK 0

1

.-

w

EXECUTIVE SUMMARY

Wolf Creek Generating Station

NRC Inspection Report 50-482/98-10

Ooerations

. A shift supervisor made an appropriate, but inadequately' documented operability

determination associated with abnormal noises from an essential service water traveling

screen (Section O4.1)

. Operations training personnel conducted effective simulator training and the staff crew

responded to the simulated steam generator tube rupture in an effective manner.

Training personnel initiated performance improvement requests (PIRs) to address the

fact that they lacked documented standards as to what constituted a complex scenario

and for what types of operator errors would require corrective action beyond that

afforded by the postscenario critique (Section 05.1).

. Licensee personnel had not monitored telephone calls to the quality first hotline between

September 13,1997, and April 1,1998 (Section O6.1).

. An operations self-assessment on the use of the operations evolution checklist identified

that the checklist was not being used consistently and in its entirety each time, yet did

not identify this as a problem. The self-assessment team's recommended actions to

. reduce the scope and level of detail of the checklist were implemented, making the

checklist less effective (Section O7.1).

. ' The licensee identified several violations of NRC requirements and reported these in

licensee event reports (LERs). These licensee-identified and corrected violations are

being treated as noncited violations, consistent with Section Vll.B.1 of the NRC

Enforcement Policy (Section 08).

Maintenance

.- The material condition of those plant systems and components evaluated during this

inspection period was good, with few equipment deficiencies. The inspectors noted an

increase in the number and severity of boric acid leaks in the auxiliary building and that

an oil leak caused an unplanned inoperability of a centrifugal charging pump

(Section M2.1).

. An arc flash event occurred during the replacement of a molded case breaker when the

breaker was not adequately disconnected from the bus. - The corrective action failed to

identify that the clearance order was incomplete in that the clearance did not establish a

boundary to isolate the breaker from the bus (Section M3.1).

l

l

l

.

-2-

Engineering

.

The inspectors found that the review level of the work package and the procedure used

to transfer an irradiated specimen was not commensurate with the potential risk to

workers involved in the transfer process. No procedure review beyond that of the

engineers working on the project was accomplished prior to the inspectors' observations

(Section E1.1).

.

Based on a review of select changes made to the Updated Safety Analysis Report,

Revision 11, the project manager determined that the changes at Wolf Creek Generating

Station have been appropriately addressed and that the changes to the Updated Safety

Analysis Report have been appropriately addressed by licensing actions,10 CFR 50.59

submittals, etc. (Section E2.1).

Plant Suonort

. Radiation protection technicians improperly posted an area with dose rates of

approximately 400 mrem /hr at 18 in. After discovery, the technicians properly posted

but failed to barricade the area (Section R1.1).

Security personnelinadvertently issued a locked high radiation area key to a radwaste

operator who was not authorized to receive the key. This licensee-identified and

corrected violation is being treated as a noncited violation, consistent with Section Vll.B.1

of the NRC Enforcement Policy (Section R1.2).

. Two contaminated area postings did not clearly describe the location of contamination on

valves (Section R1.3).

.

The inspectors found the level of the as-tow-as-reasonably-achievable (ALARA) review

cf the irradiated specimen transfer work package and procedure not commensurate with

the potential risk to workers involved in the specimen transfer process. The inspectors

determined that this was because the licensee's health physics program did not include

the potential for high exposure in the criteria for determining when an ALARA review

should be performed (Section R3.1).

u

.

4

Reoort Details

Summarv of Plant Status

The plant operated at essentially 100 percent power throughout the inspection period.

I. Operations

04 Operator Knowledge and Performance

04.1 Inadeauntelv Documented Ooerability Evaluation

a. Insoection Scona (711QZ)

The inspectors reviewed one documented Technical Specification operability screening

checklist during the inspection period.

b. Observations and Findinos

On March 6,1998, the shift supervisor completed a Technical Specification operability

screening checklist to document an operability determination performed on the Essential

Service Water Train B traveling screen. During operation, abnormal noises were heard

from the traveling screen. Maintenance personnel and the system engineer evaluated

the noise and engaged in several troubleshooting activities. Afterwards, the system

engineer stated that the noise did not affect the operability 2f the traveling screen, but

provided no basis for this conclusion. The shift supervisor completed the operability

checklist and asserted that the essential service water train was operable. The basis

statement in the operability determination described the noise and troubleshooting

activities and provided the system engineer's judgement. However, the basis statement

did not provide a tangible reason for why the noise did not represent, and could not lead

to, inoperability of the traveling screen.

After the inspector raised the question, the operations manager directed the shift

supervisor to amend the operability checklist to provide a basis. The additional

information provided an adequate basis for the operability of the traveling screen.

Operations personnel subsequently initiated PIR 98-0699 to address the recurring

concern of shift supervisors making appropriate but inadequately documented operability

determinations.

..

.

-2-

.i

1

1

i

c. Conclusions

A shift supervisor made an appropriate but inadequately supported operability

determination associated with abnormal noises from an essential service water traveling

screen.

05 Operator Training and Qualification

05.1 Simulator Trainina

a. insoection Scone (71707)

The inspectors observed a complex simulator training scenario. ,

}

b. Observations and Findinos

!

On April 2,1998, the inspectors observed a complex simulator training scenario for an '

operations staff crew. The scenario involved a steam generator tube rupture that

exceeded the available makeup rate. Operators appropriately recognized the symptoms I

and diagnosed the problem. Their response was generally appropriate. The instructor i

effectively controlled the scenario to ensure that appropriate training objectives were

accomplished.

l

The training personnel considered this scenario complex because it presented operators (

with a number of challenges, including a failure of the loss-of coolant accident J

sequencer, a stuck closed reactor trip breaker, the inability to restore instrument air to

containment, and the failure of a boron injection tank flow indicator. These challenges

occurred in a relatively linear manner and, therefore, did not present the supervising l

operator with a significant prioritization challenge. As a result, from a command and i

control standpoint, training provided a scenario that was not appreciably complex. The {

inspector asked how this scenario met the criteria to be classified as a complex scenario.  !

The operations training superintendent responded by initiating PIR 98-1249 to note and

correct the current absence of documented criteria for what constitutes a complex )

scenario. d

The instructor noted a significant emergency management guidelines procedure usage

error in that the supervising operator failed to refer to the response-not-obtained section

of Procedure EMG E-0, " Reactor Trip or Safety injection," Revision 11, associated with '

Step 1.b, to ensure that reactor trip breakers and bypass breakers were open. The.

inspector asked the operations training superintendent what corrective actions had been

taken in response to the identification of this error.. The superintendent responded that,

in this case, the instructor considered the discussion of the error during the critique to be

adequate. However, since the operations training superintendent did not have a

documented criteria to address what type of operator errors identified during training

)

I

,

k

-3-

would most appropriately be addressed solely by the critique, and when additional

actions would be needed, the superintendent initiated PIR 98-1249 to address the

absence of this criteria.

While the instructor noted several critique issues and effectively addressed them with the

crew during the critique, the inspectors identified two errors which were not discussed by

either the instructor or the crew during the critique. First, operators acknowledged

several annunciators prior to the reactor trip without referencing the associated alarm

response procedure. Second, the supervising operator reported that the leak rate

decreased when instruments indicated that the leak rate increased. The shift supervisor

apparently recognized and mentally corrected this erroneous report without specifically

discussing the matter with the supervising operator, as all operators responded to the

increasing leak rate appropriately. However, neither the operators nor the instructors

noted this communication error. .The operations training superintendent informed the

inspector that the management expectations were for instructors to note and discuss all

significant operator errors during the critiques immediately following simulator training

scenarios. The superintendent stated that this expectation will be reinforced with all

simulator instructors.

Despite the fact that the observed crew was a staP crew, the operators demonstrated

generally effective use of three-way communication. In some instances the instructor

noted communications that were not three-way; however, these were infrequent. The

inspector noted that, early in the scenario, communications were not consistently

three-way, but as the scenario progressed, the use of three-way communication became 1

more consistent,

c. Conclusions

Operations training personnel conducted effective simulator training and the staff crew

responded to the simulated steam generator tube rupture in an effective manner.

Training personnel initiated PIRs to address the fact that they lacked documented

standards for what constituted a complex scenario and for what types of operator errors

would corrective actions, beyond that afforded by the postscenario critique, be required.

06 Operations Organization and Administration

1

06.1 Quality First Teleohone System ineffective

a. Insoection Scone (71707) l

l'

The inspector evaluated the effectiveness of the quality first telephone system.

b. Observations and Findinas

On March 2,1998, the inspector telephoned the quality first telephone number and

reached the voice mail box for the quality first program. The inspector left a message

_

__ - ______ __ _____ _ _ _ - _ - _ - _____ _ ___ _ _ _

_.

.

-4-

asking a quality first representative to retum the telephone call. On April 1,1998, the

inspector noted that no retum telephone call had been made and asked wny this

occurred.

After researching the issue, licensee personnel informed the inspector that, due to a

miscommunication, the quality flrst voice mail box had not been effectively monitored

since September 13,1997. The responsibility for monitoring the quality first voice mail

box changed in September 1997, and the new person failed to receive or understand the

instructions. Consequently, the messages were not being retrieved when the person

believed that they were.

After discovering this problem, licensee personnel retrieved all messages from the voice

mail box. Only two messages had been left in the quality first voice mail box, the one

from the inspector and one from a licensee employee who asked an administrative

question but did not raise a nuclear safety concern. The licensee initiated PIR 98-0936

to address this problem and establish long-term corrective actions.

c. Conclusions

Licensee personnel had not monitored telephone calls to the quality first hotline between

September 13,1997, and April 1,1998.

07 Quality Assurance in Operations

O7.1 Ooerations Self-Assessment Not Sufficientiv Critical

a. Insoection Scooe (71707)

The inspector reviewed Self-Assessment Report SEL 98-003, " Effectiveness of the

Operations Evolution Checklist."

b. Observations and Findinas

This self-assessment reviewed the effectiveness of the operations evolution checklist, a

checklist that the licensee described as part of their corrective actions for the event

described in LER 50-482/96-008. The commitment was proceduralized in Administrative

- Procedure AP 21-001, " Operations Watchstanding Practices," Revision 6.

The self-assessment results section described interview results involving operations and

integrated plant scheduling personnel who were required by licensee procedures to use

the checklist every time certain evolutions were to begin. During these interviews, only

one person said that they used the checklist in its entirety every time, and several

individuals said that, when the workload was heavy, the use of the checklist in its entirety

each time decreased.

.

.

-5-

The inspector questioned whether this statement in the self-assessment report

suggested that licensee personnel were not complying with the procedural requirements.

Operations personnel responded that this was not what was meant by the words in the

j

i

self-assessment report. Instead, the interviewers explained that what they understood

the responses to mean was that certain steps of the checklist were not considered

applicable to certain tasks and, therefore, that that checklist element was not considered

{

applicable.

1

I

The inspector also noted that the self-assessment report recommended a revision to the 1

checklist that made it shorter and asked questions of a more general nature than the

s original checklist. The inspector determined that most cognizant individuals would be

able to envision a majority of the' elements of the proposed checklist, without the -l

prompting provided by the checklist. As a result, the revised checklist appeared to '

provide less assistance to operations than the previous checklist.

On March 20,1998, the licensee issued Administrative Procedure AP 21-001,

Revision 9, to implement the revised checklist. The shorter, less detailed checklist

recommended in the self-assessment report was implemented as recommended.

After the inspector raised questions with the self-assessment, operations personnel

initiated PIR 98-0983 to address the problem identified in the self-assessment report.

c. Conclusions

An operations self-assessment on the use of the operations evolution checklist identified

that the checklist was not being used consistently and in its entirety each time, yet did

not identify this as a problem. The self-assessment team's recommended actions to

reduce the scope and level of detail of the checklist were implemented, making the

checklist less effective.

08 Miscellaneous Operations issues (92901)

08.1 - (Closed) LER 50-482/9618-00: Failure to comply with Technical Specification

Surveillance Requirement 4.3.2.2. This item was identified when the licensee reviewed

the auxiliary feedwater system's licensing basis documentation as part of an overall

functional assessment of the auxiliary feedwater system. Technical Specification

- Requirement 4.3.2.2 for engineered safety features response-time testing required that it

be verified that the turbine-driven auxiliary feedwater pump be able to provide flow to the

steam generators within 60 seconds of an initiating signal by reaching its rated speed of

3850 rpm. The licensee noted that Surveillance Procedure STS AL-104, " Turbine Driven

9

Auxiliary Feedwater Pump Engineered Safety Features Response Time Test," verified

the turbine-driven auxiliary feedwater pump actuation response time indirectly by

measuring the turbine throttle valve stroke open time as opposed to monitoring the pump

speed directly. Two previous opportunities were identified where the licensee failed to  !

identify this error. Failure by licensee management to ensure that there were proper

mechanisms in place to verify that their standards and expectations were being met was

u

O

4

-6-

determined to be the root cause. Licensee corrective actions to mis event included the  !

'

development of a corrective action review board, changing the leadership of the plant

safety review committee, revising the surveillance procedure, and performing a sample

review of other serveillances. The described corrective actions were found to be

appropriate to address this issue. The failure by the licensee to ensure that surveillance

procedure guidance was consistent with Technical Specification requirements is a

violation of NRC requirements. This licensee-identified and corrected violation is being

treated as a noncited violation, consistent with Section Vll.B.1 of the NRC Enforcement

Policy (50-482/9810-01).

08.2 (Closed) LER 50-482/9620-00: Failure to comply with Technical Specification Action

. Statement 3.6.1.7.a. This item was identified when the licensee reviewed the draft

improved Technical Specification 3.6.1.7, " Containment Ventilation Systems," as part of

a Technical Specification improvement process, and recognized that the current

Technical Specification action statement allowed only one 3F anch containment purge

supply and/or isolation valve to be opened or not blank flanged at any one time.

Surveillance Test Procedure STS PE-015, "18-inch Purge Valve Leakage Test," which

satisfied Surveillance Requirement 4.6.1.7.4, was found to conflict with the Technical

Specification because it required the opening of both 36-inch containment purge supply

valves simultaneously. This item was identified because of the licensee's efforts to

enforce strict literal compliance with Technical Specifications. The root cause of this

. event was determined to be a misalignment between the organizational culture and the

regulatory environment.. Corrective actions taken included revising Procedure STS PE-

015, reviewing other surveillance procedures related to Technical Specification 3.6.1.7, .

providing training sessions with all departments regarding literal compliance with NRC '

requirements, and providing training to insure the proper alignment exists between the

Wolf Creek culture and the regulatory environment. The described corrective actions

were found to be appropriate for addressing this issue. The failure by the licensee to

ensure that surveillance procedure guidance was consistent with Technical Specification

requirements is a violation of NRC requirements. This licensee-identified and corrected

violation is being treated as a noncited violation, consistent with Section Vll.B.1 of the

NRC Enforcement Policy (50-482/9810-02).

08.3 (Closed) LER 50-482/9701-00. 01. 02. 03: Failure to comply with the surveillance

requirement to test certain components at shutdown. This item was identified by the-

licensee during a quality evaluations audit, during which it was questioned whether the

surveillance requirements for Technical Specification 4.7.3.b were being appropriately

met. Technical Specification 4.7.3.b stated in part that "at least two component cooling

water loops shall be demonstrated operable once per 18 months during shutdown." It

was found that portions of the Technical Specification surveillance required to be. ,

performed at shutdown were performed in Mode 1. The surveillance in question was i

performed within the appropriate time constraints set forth in the Technical l

Specifications, and the surveillance results met the acceptance criteria. A review of I

other Technical Specifications by the licensee resulted in the identification of 24 other

occurrences where surveillance tests were performed at modes other than at shutdown

contrary to Technical Specification requirements. No significant operational concerns

e-

_ _ _ . -____________ ______ - __ - _ - - ___ - -

.

.

-7-

were identified. The root cause of these events was determined to be personnel errors

made in scheduling of Technical Specification surveillances. The licensee's corrective

actions included a review of the scheduling database for similar scheduling errors,

revision of applicable procedures, and reinforcement of management expectations with

the current operations procedure writers and schedulers. The described corrective

actions were found to be appropriate for addressing this issue. The failure by the

licensee to ensure that surveillance tests were performed during the appropriate modes

of operation as required by Technical Specifications is a violation of NRC requirerrs.ts.

This licensee-identified and corrected violation is being treated as a noncited violation,

consistent with Section Vll.B.1 of the NRC Enforcement Policy (50-482/9810-03).

08.4 (Closed) LER 50-482/9704-00: Failure to accurately perform the containment integrated

leak rate test. This item was identified by the licensee. Technical Specification 4.6.1.1.d

stated that primary containment integrity shall be demonstrated by performing

containment leakage rate testing in accordance with the containment leakage rate testing

program. The licensee's Updated Safety Analysis Report indicated that, to assure leak

tight integrity, the hydrogen analyzer containment penetration valves would have to be

subjected to Type C testing and the sample lines would be opened during the Type A

test. The last Type A test, which was performed in 1991, was reviewed and it was

determined that these containment penetration valves associated with the hydrogen

analyzers were closed during the Type A test. Procedure CKL PE-018, "lLRT System

Lineups," provided erroneous guidance. The root cause of this event was determined to

be an incorrect startup procedure which was developed as part of the containment

leakage testing program. Licensee corrective actions included revising applicable

procedures, performing the required leak rate test to verify compliance with 10 CFR

Part 50, Appendix J, requirements, training of personnel, and performance of a

self-assessment of the containment integrated leak rate program. The described

corrective actions were found to be appropriate for addressing this issue. The failure by

the licensee to ensure that surveiliance procedure guidance was consistent with

Technical Specification requirements is a violation of NRC requirements. This licensee-

identified and corrected violation is being treated as a noncited violation, consistent with

Section Vll.B.1 of the NRC Enforcement Policy (50-482/9810-04).

08.5 (Closed) LER 50-482/9705-00: Violation of Technical Specification 3.8.1.1.b Emergency

Diesel Generator B. Licensee personnel, while working on an unrelated activity,

identified that the screws needed to secure the back panel of the Emergency Diesel

Generator B annunciator assembly were missing. The licensee determined that the back

panel could potentially cause the inoperability of Emergency Diesel Generator B under

seismic conditions. The root cause of this event could not be determined exactly, but

human error was considered a factor. The licensee fastened the back panel for the

Emergency Diesel Generator 8 annunciator assembly, inspected the annunciator back

panel for the Emergency Diesel Generator A, reviewed previously performed work

packages in an attempt to determine when this error occurred (no activities were

identified that would have called for the removal of the panel in question), and provided

training to maintenance craft and planning personnel to reinforce the expectations of job

completion. The described corrective actions were found to be appropriate for

!

. _ _ _ _ _ _ _ _ _ _ - _

.

.

-8-

addressing this issue. The failure by the licensee to ensure that all conditions were

appropriate for maintaining the operability of the emergency diesel generators as

required by Technical Specifications is a violation of NRC requirements. This licensee-

identified and corrected violation is being treated as a noncited violation, consistent with

Section Vll.B.1 of the NRC Enforcement Policy (50-482/9810-05).  !

08.6 (Closed) LER 50-482/9707-00. 01: Failure to procure test gas for a safety-related

component through the 10 CFR Part 50, Appendix B, program. The licensee identified

this issue while verifying prerequisite requirements for performance of Surveillance Test

Procedure STS IC-913, "CTMT Hydrogen Analyzer GS0658 Cal Test." Instrumentation

and controls technicians noticed discrepancies on the test certificates located with the

Hydrogen Analyzer B calibration test gas bottle. The licensee reviewed the appropriate

- documentation and was unable to certify the concentration of the contents of the

calibration gas bottle. Further review identified that the calibration test gas was not

purchased through the 10 CFR Part 50, Appendix B, program because originally during

plant startup the test gas was considered nonsafety-related. The root cause of this event

was determined to be personnel error la f#ng to follow Pro :edures AP 24-002,

" Requisition, Procurement Process," a9] AP 24E-001, " Identification and Control of

Materials, Parts, and Components." Lack of reconciliation of nonsafety-related material

for use in calibrating a safety-related piece of equipment has been determined to be a

contributing factor. Corrective actions taken included:

.

Performing a safety classification analysis for the hydrogen analyzer test gas

which determined that the certification process for the test gas was safety-related,

.

Performing an inspection on the vendor of the calibration gas and the licensee

issued a commercial grade dedication,

t

.

Purchasing safety-related test pas for the containment hydrogen analyzer,

.

Performing a review of other test gasses to determine if they had been

appropriately purchased (no problems were noted), and

.

Providing training to maintenance personnel involved in originating material

requisitions.

The described corrective actions were found to be appropriate for addressing this issue.

Licensee failure to follow approved procedures in purchasing material for testing

safety-related equipment is a violation of NRC requirements. This licensee-identified and

corrected violation is being treated as a noncited violation, consistent with Section Vll.B.1

of the NRC Enforcement Policy (50-482/9810-06).

08.7 (Closed) LER 50-482/9709-01: Failure to comply with Technical Specification 4.5.2.c.2.

This event was discussed in NRC Inspection Report 50-482/97-10. No new issues were

revealed by the LER.

.

.

.g.

08.8 (Closed) LER 50-482/9713-00: Section 3.7.3 Technical Specification violation regarding

two independent component cooling water loops. Licensee personnel identified that the

component cooling water loops had been cross-tied on five different occasion *, when

Procedure SYS fig-202, "CCW Surge Tank Level Equalization," was used. The

procedure guidance was found to be in error. The root cause of this event was found to

be human error in that licensee personnel failed to recognize and apply the requirem',nts

of Technical Specification 3.7.3 (which required "At least two independent component

cooling water loops shall be operable" during Modes 1 through 4) during revisims to

operating procedures which allowed cross-connecting the comoonent cooling water

surge tanks. The licensee's corrective actions included canceling Procedure

SYS EG-202 and reviewing the SYS series of operating procedures. The described

corrective actions were found to be appropriate for addressing this issue. The failure by

the licensee to ensure that surveillance procedure guidance was consistent with

Technical Specification requirements is a violation of NRC requirements. This licensee-

identified and corrected violation is being treated as a noncited violation, consistent with

Section Vll.B.1 of the NRC Enforcement Policy (50-482/9810-07).

08.9 (Closed) LER 50-482/9714-00: Waste gas system hydrogen / oxygen analyzers not

operated in accordance with Technical Specification requirements. The licensee

identified this issue when a radwaste operator, while performing a daily surveillance  ;

proceaure, questioned the acceptability of operating a waste gas system compressor j

with both hydrogen / oxygen analyzer racks being out of service. Technical l

Specifications 16.3.1.6 and 16.11.2.1.1 require that the hydrogen / oxygen analyzers be in

service at all times during waste gas holdup system operation. The root cause of this

event was determined to be inadequate administrative controls for ensuring that

analyzers were in service during system operation. Contributing factors included a lack

of clear definition of what constituted the waste gas system being in service. Licensee

corrective actions included placing the waste gas analyzers in service and revising

selected procedures to ensure that waste gas analyzers are placed in service when the

waste gas compressor is operating. The described corrective actions were found to be

appropriate for addressing this issue. The failure by the licensee to ensure that

surveillance procedure guidance was consistent with Technical Specification

requirements is a violation of NRC requirements. This licensee-identified and corrected

violation is being treated as a noncited violation, consistent with Section Vll.B.1 of the

NRC Enfcrcement Policy (50-482/9810-08).

08.10 (Closed) LER 50-482/9719-00: Failure to adequately vent emergency core cooling pump

casings and discharge piping high points in accordance with Technical Specification

Surveillance Requirement 4.5.2b.1. The licensee identified this issue following

discussions with another utility and after reviewing surveillance Procedure STS BG-002,

'ECCS Valve Check and System Vent." This procedure did not provide for venting it'e

centrifugal charging pump casings since the design of the pump did not include casing

vents. The residual heat removal pump casings had not t,9en vented in accordance with

the surveillance requirement. The root cause of this event was determined to be

personnel error on the part of the initial procedure writers in that the requirements of the

Technical Specifications were not understood or clarified before procedures were initially

L

.. . .. .. . .. .

.

. .

.

.

-10-

written or, subsequently, when they were revised. The licensee's corrective actions

included: submitting an exigent license amendment request to the NRC to revise the

surveillance requirement to require venting of only the residual heat removal and safety

injection, pump casings; reviewing isometric drawings of the residual heat removal,

safety injection, and charging systems to identify the discharge piping high point vents;

and revising Procedure STS BG-002 appropriately. The described corrective actions

were found to be appropriate for addressing this issue. The failure by the licensee to

ensure that surveillance procedure guidance was consistent with Technical Specification

requirements is a violation of NRC requirements. This licensee-identified and corrected

violation is being treated as a noncited violation, consistent with Section Vll.B.1 of the

NRC Enforcement Policy (50-482/9810-09),

ll. Maintenance

M1 Conduct of Maintenance

M1.1 General Comments on Maintenance Activities

a. Insoection Scoce (72707)

The inspectors observed all or portions of the following work activities.

WP 101433 Task 8 NG01 A CR2 molded case breaker replacement

WP 120634 Task 1 Motor-operated valve preventive maintenance on

EJ FCV610

WP 123484 Task 1 Motor-operated valve preventive maintenance on

BN HV8812A

WP 101435 Task 14 NG02A remove existing breaker and install

Westinghouse breaker

WP 112855 Task 2 Replace Pump PAN 01A

WP 126639 Task 1 Irradiated specimen transfer

b. Observation and Findinas  ;

!

Except as noted in Sections M2.1 and M3.1, the inspectors found no concerns with the

maintenance observed.

4

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ - .

.

.

-11-

c. Conclusions

Except as noted in Sections M2.1 and 3.1, the inspectors concluded that the

maintenance activities were being performed as required.

M1.2 General Comments on Surveillance Activities

a. Insoection Scone (61726)

The inspectors observed all or portions of the following surveillance activities.

STS EG-201A, Revision 3 Component cooling water system Train A inservice valve

test

STS EN-1008, Revision 11 Containment Spray Pump B inservice pump test

STS KJ-005A, Revision 30 Manual / Auto start, synchronization loading of Emergency

Diesel Generator NE01

STS RE-015, Revision 2 Irradiated surveillance specimens

STS SE-001, Revision 21 Power range adjustment to calorimetric

b. Observations and Findinas

The inspectors found no concerns with the surveillances observed.

c. Conclusions

The inspectors concluded that the surveillance activities were being performed as

required.

M2 Maintenance and Material Condition of Facilities and Equipment

M2.1 Review of Material Condition Durina Plant Tours

a. Insoection Scooe (61726)

During this inspection period, routine plant tours were conducted to evaluate plant

material condition.

b. Observations and Findinas

in general, where equipment deficiencies existed, the deficiencies had been identified by

the licensee for corrective action.

- . _ . ______

______ _-__ -__-_____ ___-___-_____--_ _ __ _ _ _ _ __

1

.

-12-

.

During this inspection period, the inspectors noted an increase in the number and

severity of boric acid leaks from valves, flanges, and components in the safety

injection pump rooms, centrifugal and normal charging pump rooms, residual

heat removal heat exchanger rooms, and the mechanical penetration rooms over

conditions that existed previously. The inspectors noted that the licensee han

taken action to correct this trend.

.

The inspectors noted that the condition of the Class 1E air conditioning unit

(SGK 05A/B) discharge valves was degrading due to worsening corrosion in the

bonnet area.

.

On March 30,1998, an oil leak on Centrifugal Charging Pump B resulted in an

unplanned entry into a limiting conditions for operation action statement due to

the pump being inoperable. The inspectors noted that the licensee restored the

system to operable status promptly and appropriately.

F

c. Conclusions

The material condition of those plant systems and components evaluated during this

inspection period was good, with few equipment deficiencies. The inspectors noted an

increase in the number and severity of boric acid leaks in the auxiliary building and that

an oilleak caused an unplanned inoperability of a centrifugal charging pump.

M3 Maintenance Procedures and Documentation

M3.1 Molded Case Breaker Arc Flash Event

a. Insoection Scoos (62703)

The inspector reviewed the licensee's response to an arc flash event that occurred

during a molded case circuit breaker replacement.

b. Observations and Findinas

On March 17,1998. during the replacement of a molded case circuit breaker in an ITE

Gould Series 5600 motor control center, the electrician removed the 24 inch

self-contained control unit and relied on the dogs to prevent the control unit from moving

inward and contacting the energized bus. While tightening the screws at the top of the

breaker, the electrician exerted sufficient force on the self-contained control unit to cause

it to flex, which closed the gap and caused the contacts to touch the bus. This created

an electrical current path from the bus to the control unit contacts, through the wires to

the line side breaker terminals, up the electrician's screwdriver shaft, to a bracket holding

the breaker, to the control uriit metal housing, to the control unit dogs, to the motor

control center frame, to ground. In the process, an arc occurred at several points along

this path, including one between the electrician's screwdriver and th~ e breaker mounting

{

.

1

.

.

I

-13-

bracket and one which welded the control unit dog to the motor control center frame.

The screwdriver arc caused a flash burn to the electrician's finger. The electrician was

given first aid and permitted to return to work.

The licensee initiated a safety investigation which identified that the electrical isolation for

the control unit was not adequate. By relying on the dogs to prevent inward movement

of the control unit, the gap between the contacts on the back of the control unit and the

bus was approximately 1/4 inch. A:, demonstrated by this event, control unit flexure can

be large enough to close this gap and bridge the presumed electrical isolation.

The vendor technical manual procedure for locking out these control units for

maintenance described 3/8-inch holes in the motor control center slide rail and in the

control unit. With these holes aligned, the clearance between the bus and the control

unit contact increased 7/8 inch beyond the clearance provided by reliance on the dogs.

The licensee discussed this event with several other utilities and determined that every 1

utility they contacted had been isolating motor control center control units in the same )

manner and were similarly unfamiliar with the vendor technical manual guidance  !

regarding the control unit lockout position. NRC Morning Report 4-98-0013 provides an

initial overview of this event. The licensee reported this event to the LJustry through the

institute for Nuclear Power Operations and is evaluating other means to r ommunicate

this information more widely.

The licensee revised the maintenance procedure for these breakers to require

electricians to slide the control unit out sufficiently so these lockout holes align and to

install a locking device that prevents inward movement.

The inspector noted that the licensee's investigation did nd specifically conclude that the

clearance order for this work was inappropriate. The inspector reviewed the clearance ,

order for this breaker replacement. The clearance order required that the breaker be l

l

tagged open, but provided no boundary to isolate the molded case breaker from the bus.

When the inspector asked clearance order personnel why this clearance order did not

establish isolation of the molded case breaker from the bus, they replied that it was their

standard practice to rely on the electrician's skill of the craft and on the procedure to

isolate the breaker from the bus before de-terminating it. The inspector reviewed the

licensee's program for working on known energized equipment. The program only

applies to circuits with voltages exceeding 277 volts and only applies to work involving

planned contact of the electrician's hand or tools with known energized conductors.

Since the electricians planned to slide the control unit out prior to de-terminating the

l

breaker, they did not plan to work on energized equipment and, therefore, this program

did not apply.

The inspector reviewed Procedure AP 21E-001, " Clearance Orders," Revision 6, and

noted that the procedure purpose statement read "This procedure provides a tagging

method to ensure personnel safety and equipment protection during all plant conditions."

The inspector questioned whether the clearance order procedure specifically required

i

.

6

-14-

t

components to be replaced to be completely isolated from energy sources. The

inspector also questioned whether the clearance order procedure permitted issuance of

clearance orders that did not provide complete isolation and, therefore, protection of

personnel and equipment. Finally, the inspector questioned whether there was a

provision in the clearance order program for the preparer to intentionally not completely

isolate a component and visibly invoke some sort of other administrative controls to

- ensure that these other controls provided the protection not provided by the clearance

order. These questions were still open at the end of the inspection period, and these

issues will be tracked as an unresolved item until these questions are answered

(50-482/9810-10).

c. Conclusions

An arc flash event occurred during the replacement of a molded case breaker when the

breaker was not adequately disconnected from the bus. The corrective action failed to

identify that the clearance order was incomplete in that the clearance did not establish a

boundary to isolate the breaker from the bus.

Ill. Engineering

E1 Conduct or Engineering

E1.1 Enoineerina Daartment Review of Irradiated Soecimen Transfer Work Packaoe

a. Insoection Scooe (37551)

The inspector reviewed engineering department activities associated with transfer of an

irradiated specimen from the spent fuel pool to a shipping cask.

b. Observations and Findinas

On March 25,1998, the inspector observed engineering, operations, and health physics

personnel prepare to accomplish movement of an irradiated reactor vessel specimen

from the spent fuel pool, where it had been stored since Refueling Outage 9, to a

shipping cask along side the pool. The evolution was accomplished using Work

Package 126639, Irradiated Specimen Transfer, Task 1, and Procedure STS RE-015,

' irradiated Surveillance Specimens," Revision 2.

The irradiated specimen transfer process had been accomplished twice before this time,

most recently in December 1991. This infrequent task involved raising the irradiated 1

specimen from the spent fuel pool using the spent fuel pool crane and lowering the

specimen into a shipping cask with a narrow (just-the-right-size) opening. This process

was complicated by the fact that high radiation doses from the specimen (40R/hr)

required the operators to perform this operation from a distance using a television

monitor in order to reduce their radiation dose. Further complications were encountered

L

.

.

-15-

when the gripper used to grapple the irradiated specimen in the spent fuel pool did not

match the connection points on the' specimen liner. Despite these complicating factors

and the potential for high doses should a problem have been encountered, no procedure

review beyond that of the engineers working on the project was accomplished prior to the

inspectors observations.

The inspectors found that the level of review of the work package and the precedure

used to transfer the irradiated specimen was not commensurate with the potential risk to

workers involved in the transfer process. The inspector also determined that the

installed funnel used to guide the specimen into the shipping cask was not addressed in

the work package or in the procedure. Questions asked by the inspector resulted in a

change being made to the procedure to address use of the funnel as a guide for the

specimen.

c. Conclusions

The inspectors found that the level of review of the work package and the procedure

used to transfer an irradiated specimen was not commensurate with the potential risk to

workers involved in the transfer process. No procedure review beyond that of the

engineers working on the project was accomplished prior to the inspectors' observations.

E2 Engine *, ring Support of Facilities and Equipment .

E2.1 Review of Wolf Creek Generatina Station Annual Safety Evaluation Reoort and Final '

Safety Analvsis Reoort Uodate

a.- Insoection Scooe (37551)

By letters dated March 11,1998, Wolf Creek Nuclear Operating Corporation submitted

the Wolf Creek Generating Station Annual Safety Evaluation Report and the Wolf Creek

Updated Safety Analysis Report (USAR), Revision 11. During the week of March 23,

1998, the NRC project manager performed a review of the annual safety evaluation  !

report on a sampling basis to assess whether the licensee's submittal clearly described

the changes in sufficient detail to determine if the licensee's conc;usion that the changes

did not involve an unreviewed safety question appeared reasonable. In addition, the {

NRC project manager performed a review of Revision 11 to the USAR on a sampling J

basis to determine if: (1) changes at the Wolf Creek Generating Station have been ]

appropriately addressed in the USAR, and (2) changes to the USAR have been I

appropriately addressed by licensing actions,10 CFR 50.59 submittals, etc.

b. Observations and Findinas

The project manager determined that the safety evaluation summaries in the annual

safety evaluation report that were reviewed were of high quality and contained sufficient

detail to determine if the licensee's conclusion that the changes did not involve an

I

L h

.

..

-16-

unreviewed safety question appeared reasonable. A review, on a sampling basis, of the

safety evaluations summarized in the annual safety evaluation report, will be performed

during the next 10 CFR 50.59 inspection.

. ConclusiODE

Based on a review of select changes made to the USAR, Revision 11, the project

manager determined that the changes at Wolf Creek Generating Station have been

appropriately addressed in the USAR and that the changes to the USAR have been

appropriately addressed by licensing actions,10 CFR 50.59 submittals, etc.

IV. Plant Support

R1 Radiological Protection and Chemistry Controls

R1.1 Inadeouate Hiah Radiation Area Postina

a. Insoection Scone (71750) j

The inspector reviewed the licensee's response to the discovery of an inappropriately

posted high radiation area.

b. Observations and Findinas

l

On April 10,1998, a radiation protection supervisor noted that health physics technicians

posted the entrance to scaffolding up to the roof of the new radwaste storage building as  !

a radiation area. The supervisor questioned whether the radwaste building roof was

.

]

accessible from the roof of the new radwaste storage building. The survey map that I

supported the posting for the new radwaste storage building showed radiation levels at i

the edge of the new radwaste storage building had been 60 mrem per hour and also )

showed that the technicians had not documented surveying the roof of the radwaste ]

building. The subsequent investigation revealed that the technicians had not surveyed )

the roof of the radwaste building and that it would be easy to step from the new radwaste t

storage building roof to the radwaste building roof. Subsequent surveys showed that I

radiation levels on the radwaste building roof were approximately 400 mrem per hour "

at 18 in.

After recognizing that the high radiation area was not posted appropriately, the radiation

protection supervisor directed the technicians to post the area as a high radiation area.'

Later that evening, a radiation protection supervisor reviewed the posting again and

recognized that, while the area had been posted as a high radiation area, it had not been

barricaded. The supervisor barricaded the area immediately with yellow and maconta

rope. Later, radiation protection supervisors initiated PIRs 98-1027 and -1028 to address

these issues.

E

.

.

-17-

Technical Specification 6.12 required this area to be posted as a high radiation area and

barricaded. The failure of technicians to properly post and barricade this area are two

examples of a violation of Technical Specification 6.12 (50-482/9810-11).

c. Conclusions

Radiation protection technicians improperly posted an area with dose rates of

approximately 400 mrem /hr at 18 in. After discovery, the technicians properly posted

but failed to barricade the area.

R1.2 Locked High Radiation Area Kev Issued Inanorooriatelv

a. Insoection Scooe (71750)

The inspector reviewed the licensee's actions following their discovery of an instance in

which a locked high radiation area key was issued without the approval of radiation

protection personnel.

b. Observations and Findings

On April 10,1998, security personnelissued the locked high radiation area keys to a

radwaste operator inappropriately in that they did not have the permission of radiation  ;

protection p;rsonnel. Security Procedure 01-206, "High Security Key Control and Issue,"

Revision 23, required that locked high radiation area keys only be issued to individuals

listed on the authorized list kept at the secondary alarm station. Only radiation protection-

technicians and their supervisors were on the authorized list.

Security personnel recently reorganized their key storage. The locksmith provided a

reminder to all security sergeants and lieutenants that keys were being reorganized anci

that additional effort would be needed in the area of self-checking and attention to detail.

However, the sergeant who issued the key did not ask the radwaste operator which key

was needed and did not carefully check to ensure that the key issued was the one

intended.

Immediate corrective actions included contacting the radwaste operator, retrieving the

' locked high radiation area key, obtaining a voluntary statement from the radwaste

operator, notifying radiation protection personnel, and briefing all key issue officers

regarding the event and the importance of issuing keys properly. The security lieutenant

initiated PIR 98-1029 to address longer-term corrective actions. One longer-term

corrective action that was completed within a few days of the event was to attach yellow

and magenta tags to each locked high radiation area key to readily identify these keys.

While the radwaste operator entered the radiologically controlled area with the locked

high radiation area key for shift turnover, according to the voluntary statement, the key

was never used to access locked high radiation areas.

1

& )

-

.

i

-

\

'

-18-

I

1

The inappropriate issuance of a locked high radiation area key is a violation of Technica! l

Specification 6.11. This licensee-identified and corrected violation is being treated as a

noncited violation, consistent with Section Vll.B.1 of the NRC Enforcement Policy

(50-482/9810-12).

c. Conclusions )

Security personnel inadvertently issued a locked high radiation area key to a radwaste l

opcrator who was not authorized to receive this key. )

1

R1.3 Unclear Contaminated Area Postings

I

a. Insoection Scooe (71750) )

l

Throughout this inspection period, during tours in the radiologically controlled area, the

inspectors observed various radiation protection postings.

b. Observations and Findinas l

l

On April 3,1998, the inspector noted contaminated area postings for l

Valves EJ HV8816A and -B, the residual heat removal discharge cross tie to reactor j

coolant system hot leg injection. These postings warned that there was a contaminated '

area "inside valve body." The inspector asked the lead health physics technician what

these postings meant and was informed that there was a packing leak and that the

contaminated area was on the valve body in the valve stem packing area.

The lead radiation protection technician subsequently reposted the valves to more clearly j

describe the proper location of the contaminated area. Radiation protection supervision

also stated that this issue would be reinforced during future discussions with all radiation ]

protection technicians. J

c. Conclusions  ;

I

Two contaminated area postings did not clearly describe the location of contamination on i

valves.

l

R3 Radiological Protection and Chemistry Procedures and Documentation  !

l

R3.1 Radiation orotection ALARA Review of Irradiated Soecimen Transfer Procedure

a. Insoection Scooe (71750)

The inspector reviewed radiation protection department activities associated with transfer

of an irradiated specimen from the spent fuel pool to the shipping cask.

k

-.

.

-19-

b. Observations and Findinas

l

On March 25,1998, the inspector observed engineering, operations, and radiation

protection personnel prepare for and attempt to accomplish movement of an irradiated

reactor vessel specimen from the spent fuel po% w here it had been stored since

Refueling Outage 9, to a shipping cask along sie the pool. The radiological controls I

were established in Radiation Work Permit 980087, Revision 1.

The irradiated specimen transfer process had been accomplished twice before this time,

(nost recently in December of 1991. This infrequent task involved raising the irradiated

specimen from the spent fuel pool using the spent fuel pool crane and lowering the

specimen into a shipping cask with a narrow (just-the-right-size) opening. This process

_

was complicated by the fact that high radiation doses from the specimen (40R/hr)

required that operators and radiation protection support personnel perform their function

from a distance in order to prevent high doses and to reduce their radiation doses.

Procedure AP 16C-003, " Work Package Task Planning," Revision 5, paragraph 6.5.2.11,

refers the work package planner to Procedure AP 25B-300, "RWP Program," Revision 6,

to use a " Pre-Job ALARA Checklist" if the work was to be accomplished in the

radiological controlled area. Procedure AP 258-300, paragraph 5.4, requires that prejob

ALARA checklists be performed only when estimated doses were expected to be equal

or greater than one person-rem. The estimated doses for the irradiated specimen

transfer were less than one person-rem, though the contingency plan in the event that

the specimen became stuck while being inserted into the shipping cask included sending

an individual up on a ladder to grasp the specimen by hand to physically assist inserting

the specimen into the cask. If the this planned contingent action had been called upon,

the exposure for the entire specimen transfer could have exceeded the one person-rem

criteria for an ALARA review. Despite this contingency plan and the potential for high

doses should a problem have been encountered, no ALARA review per

Procedure AP 258-300 was performed.

'The inspectors found that the level of ALARA review of the work package and the

procedure used to transfer the irradiated specimen was not commensurate with the

potential risk to workers involved in the specimen transfer process. The inspectors

determined that this was partly a result of Procedure AP 25B-300 not including potential

exposure in the criteria for determining when an ALARA review should be performed.

The inspectors noted that the radiation protection department started reviewing these

procedures and policy for possible correction.

c. Conclusions

The inspectors found that the level of ALA RA review of an irradiated specimen transfer

work package and procedure was not con mensurate with the potential risk to workers

involved in the specimen transfer process. The inspectors determined that this was

1

!

i_

P-

O

,

'

-20-

because the licensee's radiation protection program did not include the potential for high

exposure in the criteria for determining when an ALARA review should be performed

(Section 3.1).

V. Manaaement Meetinas

X1 Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at the '

conclusions of the inspection on April 17,1998. The licensee acknowledged the findings l

presented.

l

l

The inspectors asked the licensee whether any materials examined during the inspection should I

be considered proprietary. No proprietary information was identified.

j

-

.

,

4

6

SUPPLEMENTAL INFORMATION

PARTIAL LIST OF PERSONS CONTACTED

Licensee

M. J. Angus, Manager, Licensing and Corrective Action

G. D. Boyer, Chief Administrative Officer

J. W. Johnson, Manager, Resource Protection

O. L. Maynard, President and Chief Executive Officer

B. T. McKinney, Plant Manager

R. Muench, Vice President Engineering

]

W. B. Norton, Manager, Performance improvement and Assessment 1

C. C. Warren, Chief Operating Officer )

1

INSPECTION PROCEDURES USED

IP 37551 Onsite Engineering

IP 61726 Surveillance Observations

IP 62707 Maintenance Observations

IP 71707 Plant Operations

IP 71750 Plant Support Activities

IP 92901 Followup - Operations

ITEMS OPENED AND CLOSED

Ooened

50-482/9810-01 NCV Failure to comply with Technical Specification Surveillance

Requirement 4.3.2.2 (Section 08.1)

1

50-482/9810-02 NCV Failure to comply with Technical Specification Action 1

Statement 3.6.1.7.a (Section 08.2)

50-482/9810-03 NCV Failure to comply with surveillance requirement to test

certain components at shutdown (Section 08.3)

50-482/9810-04 NCV Failure to accurately perform the containment integrated

leak rate test (Section 08.4)

50-482/9810-05 NCV Violation of Technical Specification 3./8.1.1., Emergency

Diesel Generator B (Section 08.5) l

50-482/9810-06 NCV Failure to procure test gas for a safety-related component

through an Appendix B program (Section 08.6)

I

+-

.

4

4

.

-2-

50-482/9810-07 ~ NCV Section 3.7.3 Technical Specification violation regarding two

independent component cooling water loops (Section 08.8) 'l

50-482/9810-08 NCV Waste gas system hydrogen / oxygen analyzers not operated

in accordance with Technical Specification requirements

(Section 08.9)

50-482/9810-09 NCV Failure to adequately vent emergency core cooling pump

casings and discharge piping high points in accordance with

Technical Specification Surveillance Requirement 4.5.2b.1

(Section 08.10)

50-482/9810-10 URI Molded case breaker are flash event (Section M3.1)

50-482/9810-11 VIO Inadequate high radiation area posting (Section R1.1)

50-482/9810-12 NCV Locked high radiation area key issued

inappropriately (Section R1.2)

Closed

50-482/9618-00 LER Failure to comply with Technical Specification Surveillance

Requirement 4.3.2.2 (Section 08.1)

50 482/9620-00 LER Failure to comply with Technical Specification Action

Statement 3.6.1.7.a (Section 08.2)

50-482/9701-00, LER Failure to comply with surveillance requirement to test certain

01,02,03 components at shutdown (Section 08.3) -

50-482/9704-00 LER Failure to accurately perform the containment integrated leak

rate test (Section 08.4)

50-482/9705-00 LER Violation of Technical Specification 3.8.1.1, Emergency

Diesel Generator B (Section 08.5)

- 50-482/9707-00, LER. Failure to procure test gas for a safety-related component

.01- through an Appendix B program (Section 08.6)

50-482/9709-01 LER Failure to comply with Technical Specification 4.5.2.c.2

(Section 08.7)

50-482/9713-00 LER Section 3.7.3 Technical Specification violation regarding two

independent component cooling water loops (Section 08.8)

- 50-482/9714-00 LER Waste gas system hydrogen / oxygen analyzers not operated

in accordance with Technical Specification requirements

(Section 08.9)

L-

.

4

4

..

3-

50-482/9719-00 LER Failure to adequately vent emergency core cooling pump

casings and discharge piping high points in accordance with

Technical Specification Surveillance Requirement 4.5.2b.1

(Section 08.10)

50-482/9810-01 NCV Failure to comply with Technical Specification Surveillance

Requirement 4.3.2.2 (Section 08.1)

50-482/9810-02 NCV Failure to comply with Technical Specification Action

Statement 3.6.1.7.a (Section 08.2)

50-482/9810-03 NCV Failure to comply with surveillance requirement to test certain

components at shutdown (Section 08.3)

50-482/9810-04 NCV Failure to accurately perform the containment integrated leak

rate test (Section 08.4)

50-482/9810-05 NCV Violation of Technical Specification 3.8.1.1, Emergency

Diesel Generator B (Section 08.5)

50-482/9810-06 .NCV Failure to procure test gas for a safety-related component

through an Appendix B program (Section 08.6)

50-482/9810-07 NCV Section 3.7.3 Technical Specification violation regarding two

independent component cooling water loops (Section O8.8)

50-482/9810-08 NCk Waste gas system hydrogen / oxygen analyzers not operated

in accordance with Technical Specification requirements

(Section 08.9)

50-482/9810-09 NCV Failure to adequately vent emergency core cooling pump

casings and discharge piping high points in accordance with

Technical Specification Surveillance Requirement 4.5.2b.1

(Section 08.10)

50-482/9810-12 NCV Locked high radiation area key issued

.

inappropr'ately (Section R1.2)

i

,