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{{#Wiki_filter:NRC FORM 366 (7 77)LICENCEE EVENT REPORT CONTROL BLOCK: l llllllh (PLEASE PRINT OR TYPE A11LREQUIRED INFORMATION) 1 6[oTil Ic I A IE 11 in 11 l@l 010101010101010101010 I@2641111ililll@l Il@7 8 9 LICENSEE CODE le 15 LICENSE NUMBER 23.laCENSE TYPE JO
{{#Wiki_filter:NRC FORM 366 (7 77)
$7 CAT 68.CO.lL l@l0 l5 l0 l0 10 l3 l2 l1 @l 1 l 1 l 2 8l 7l 9 @l 1 2 l 1l 1l. 7 l 9 l@
LICENCEE EVENT REPORT CONTROL BLOCK: l 1
'0 1 5 VRC 7 8 60 6l DOCKET NUMBER 68 69 EVENT OATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h lO l2l l Af ter re-calibration of P33-P001A and B during steady state power operation, it lIO lal l was observed that the Drywell-Torus H2 and 02 Analyzers "A zud B" were indicating lo 4lgreater than 4% oxygen concentration. The samples taken by lab instrumentation lo 5 lrevealed that the oxygen concentration was 3%.
l      l    l    l    l lh 6
There was no effect on the environs. l O cl This was a non-repetitive event.
(PLEASE PRINT OR TYPE A11LREQUIRED INFORMATION)
ll O s lJ i_80 7 8 9 E CODE SUSCO E COMPONENT CODE SUSOdE SU E[ O].9_jl SjA h b h lX lh l P ! E I N l E l T l R lh J@ y @
[oTil8 Ic 7          9 I A         IE 11 LICENSEE    CODEin 11 l@l 010101010101010101010 le    15                        LICENSE NUMBER                  23 I@2641111ililll@l
7 8 9 10 11 12 13 18 19 20_SEQUENTI AL OCCUR R E NCE RiPORT REVISION LE R 'RO EVENT YE AR REPORT NO.
                                                                                                                                      .laCENSE TYPE JO I
CODE TYPE NO.h REl7l9[--J 0 l 9 l7 l Ml0 3ll Lll_][ 0_j yu_ 21 22 23 24 26 27 28 29 JD 31 32 K N AC ON ON PLA T E HOURS SB IT FO B.SUPPLIER MAN FACTURER l El@lZ l@
                                                                                                                                                                $7 CAT 68 l@
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CO.
33 34 35 36 3/40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i O l The cause of the occurrence has been attributed to air inlerkage to the annlyzers li i j causing them to observe a higher than actual reading.
0 1 5 VRC      lL   l@l0 l5 l0DOCKET          l0 10           l3 l2 l1 @l   68 1 l 1EVENT 69 l 2 OATE8l 7l 9 74@l 1 2REPORT75 l 1l 1l. 7 l 980l@
The Eines were tested and l, 7 lall identified leaks repaired.The analyzers were re-calitrated and returned li 3 lto service.
DATE 7       8                     60           6l                         NUMBER EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h lO l2l l Af ter re-calibration of P33-P001A and B during steady state power operation, it                                                                                       l IO lal l was observed that the Drywell-Torus H2 and 02 Analyzers "A zud B" were indicating                                                                                       l o 4      l greater than 4% oxygen concentration. The samples taken by lab instrumentation                                                                               l o 5 l          revealed that the oxygen concentration was 3%.                                                 There was no effect on the environs. l O c      l This was a non-repetitive event.                                                                                                                                 l O   s l                                                            J  i  _
ll1 4 7 8 9 80 ST S% POWER OTHER STATUS IS O RY DISQVERY DESCRIPTION l1 l51lE @
l 80 7       8 9 E               CODE         SUSCO E                   COMPONENT CODE                 SUSOdE           SU     E
0l 9 l 8l@l NAll B l@lObservation lACTIVITY CO TENT RELEASED OF RELE ASE AMOUNT OF ACTIVITY LOCA10N QF RELEASE NAllNel] @ [_Zj@l 1 6 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBE R TYPE DESCRIPTION W 10 l 0 l 0 l@l Z l@l NA''' PERSONNEL INJU IES mSCR P1,0~8 1592 236 NUM ER NAl10l0l0l@l1 a 7 8 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY TYPE DESCRIPil0N b [Z_j@lNAl7 tl 9 to 80"'''o'ESCniPriON@
[ O].9_j                          l SjA h b h lX lh l P ! E I N l E l T l R lh J@ y @
7 91217 0 3/4,l'*NnC usE ONtv iSSu@lNAlllllllllll;2 o 7 8 9 10 68 69 80 E NAME OF PREPARER PHONE**
9                                                                                      18          19              20 7       8                                   10           11               12             13
1-NARRATIVE REPORT Georgia Power Company' Plant E.I. llatch Baxley, Georgia Reportable Occurrence Report No. 50-321/1979-097 Af ter re-calibration of P33-P001A and B during steady state power operation analyzers "A and B" at 98% power, J t was observed that the drywell-torus H 022 were indicating greater than 4% oxygen concentration. Actual drywell samples revealed the oxygen concentration was 3%.
_                                                SEQUENTI AL                     OCCUR R E NCE         RiPORT                   REVISION EVENT YE AR                                   REPORT NO.                         CODE               TYPE                     NO.
There was no affect on the environs. This was a non-repetitive event. The cause of the occurrence has been attributed to air inleakage to the analyzers causing them to observe a higher than actual reading. The lines were isolated and pressurized, several leaks in the panel were found and repaired. The analyzers were re-calibrated and returned to service. This problem is only applicable to Unit I because the Unit II drywell is. not inerted. The analyzers are not utilized on any other safety related system on either unit.
LE R 'RO h RE  yu
1592 237-e}}
_ 21 l7l9 22
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27 l0 3l 28       29 l Ll JD l_]
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[ 0_j 32 K N AC ON                 ON PLA T               E                         HOURS           SB IT           FO       B. SUPPLIER           MAN FACTURER l33El@lZ   34 l@           l35Z l@           W@
36                  3/
0l0l0l0l 40 W@
41              42 Nl@             lNl@
43 lXl9l9l9l@
44             47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i O l The cause of the occurrence has been attributed to air inlerkage to the annlyzers                                                                                     l i i     j     causing them to observe a higher than actual reading.                                                       The Eines were tested and                       l
    , 7 l          all identified leaks                           repaired.             The analyzers were re-calitrated and returned                                           l i 3 l          to service.                                                                                                                                                 l 1 4                                                                                                                                                                         l 7     8 9                                                                                                                                                                   80 ST     S           % POWER                         OTHER STATUS                   IS O RY                           DISQVERY DESCRIPTION NA                                        Observation l1 l51lE @                     0l 9 l 8l@l                                                 l    l B l@l                                                                      l ACTIVITY CO TENT RELEASED OF RELE ASE                           AMOUNT OF ACTIVITY                                                       LOCA10N QF RELEASE 7
1 6 8 9
            ] @ [_Zj@l       10           11 NA 44 l          l 45 Ne 80 l
PERSONNEL EXPOSURES NUMBE R             TYPE           DESCRIPTION NA W 10 l 0 l 0 l@l Z l@l
            ' PERSONNEL INJU IES NUM ER              mSCR P1,0~8                                                                                             1592 236 7
1 a 8 9 10l0l0l@l        11     12 NA 80 l
LOSS OF OR DAMAGE TO FACILITY TYPE       DESCRIPil0N b [Z_j@l                                                                                            NA                                                                        l 7      tl 9             to                                                                                                                                                 80 iSSu
                    "'''o'ESCniPriON@                                                                     7 91217 0 3/4,                                   NnC usE ONtv 2 o              @l                                                                              NA                                        l        llllll        lllll; 7       8 9             10                                                                                                                   68 69                         80 E NAME OF PREPARER PHONE
 
1 NARRATIVE REPORT Georgia Power Company' Plant E. I. llatch Baxley, Georgia Reportable Occurrence Report No. 50-321/1979-097 Af ter re-calibration of P33-P001A and B during steady state power operation at 98% power, J t was observed that the drywell-torus H 022 analyzers "A and B" were indicating greater than 4% oxygen concentration. Actual drywell samples revealed the oxygen concentration was 3%. There was no affect on the environs. This was a non-repetitive event. The cause of the occurrence has been attributed to air inleakage to the analyzers causing them to observe a higher than actual reading. The lines were isolated and pressurized, several leaks in the panel were found and repaired. The analyzers were re-calibrated and returned to service. This problem is only applicable to Unit I because the Unit II drywell is. not inerted. The analyzers are not utilized on any other safety related system on either unit.
1592 237 e}}

Latest revision as of 04:57, 2 February 2020

LER 79-097/03L-0:on 791128,after Recalibr of P33-P001A & B During Steady State Power Operation,Drywell Torus Dihydrogen & Dioxide Analyzers a & B Indicated More than 4% Oxygen Concentration.Caused by Leakage of Air Into Analyzer
ML19211A290
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 12/11/1979
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19211A280 List:
References
LER-79-097-03L-01, LER-79-97-3L-1, NUDOCS 7912170316
Download: ML19211A290 (2)


Text

NRC FORM 366 (7 77)

LICENCEE EVENT REPORT CONTROL BLOCK: l 1

l l l l l lh 6

(PLEASE PRINT OR TYPE A11LREQUIRED INFORMATION)

[oTil8 Ic 7 9 I A IE 11 LICENSEE CODEin 11 l@l 010101010101010101010 le 15 LICENSE NUMBER 23 I@2641111ililll@l

.laCENSE TYPE JO I

$7 CAT 68 l@

CO.

0 1 5 VRC lL l@l0 l5 l0DOCKET l0 10 l3 l2 l1 @l 68 1 l 1EVENT 69 l 2 OATE8l 7l 9 74@l 1 2REPORT75 l 1l 1l. 7 l 980l@

DATE 7 8 60 6l NUMBER EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h lO l2l l Af ter re-calibration of P33-P001A and B during steady state power operation, it l IO lal l was observed that the Drywell-Torus H2 and 02 Analyzers "A zud B" were indicating l o 4 l greater than 4% oxygen concentration. The samples taken by lab instrumentation l o 5 l revealed that the oxygen concentration was 3%. There was no effect on the environs. l O c l This was a non-repetitive event. l O s l J i _

l 80 7 8 9 E CODE SUSCO E COMPONENT CODE SUSOdE SU E

[ O].9_j l SjA h b h lX lh l P ! E I N l E l T l R lh J@ y @

9 18 19 20 7 8 10 11 12 13

_ SEQUENTI AL OCCUR R E NCE RiPORT REVISION EVENT YE AR REPORT NO. CODE TYPE NO.

LE R 'RO h RE yu

_ 21 l7l9 22

[--J 23 24 0 l 9 l7 l 26 M

27 l0 3l 28 29 l Ll JD l_]

31

[ 0_j 32 K N AC ON ON PLA T E HOURS SB IT FO B. SUPPLIER MAN FACTURER l33El@lZ 34 l@ l35Z l@ W@

36 3/

0l0l0l0l 40 W@

41 42 Nl@ lNl@

43 lXl9l9l9l@

44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i O l The cause of the occurrence has been attributed to air inlerkage to the annlyzers l i i j causing them to observe a higher than actual reading. The Eines were tested and l

, 7 l all identified leaks repaired. The analyzers were re-calitrated and returned l i 3 l to service. l 1 4 l 7 8 9 80 ST S  % POWER OTHER STATUS IS O RY DISQVERY DESCRIPTION NA Observation l1 l51lE @ 0l 9 l 8l@l l l B l@l l ACTIVITY CO TENT RELEASED OF RELE ASE AMOUNT OF ACTIVITY LOCA10N QF RELEASE 7

1 6 8 9

] @ [_Zj@l 10 11 NA 44 l l 45 Ne 80 l

PERSONNEL EXPOSURES NUMBE R TYPE DESCRIPTION NA W 10 l 0 l 0 l@l Z l@l

' PERSONNEL INJU IES NUM ER mSCR P1,0~8 1592 236 7

1 a 8 9 10l0l0l@l 11 12 NA 80 l

LOSS OF OR DAMAGE TO FACILITY TYPE DESCRIPil0N b [Z_j@l NA l 7 tl 9 to 80 iSSu

"o'ESCniPriON@ 7 91217 0 3/4, NnC usE ONtv 2 o @l NA l llllll lllll; 7 8 9 10 68 69 80 E NAME OF PREPARER PHONE

1 NARRATIVE REPORT Georgia Power Company' Plant E. I. llatch Baxley, Georgia Reportable Occurrence Report No. 50-321/1979-097 Af ter re-calibration of P33-P001A and B during steady state power operation at 98% power, J t was observed that the drywell-torus H 022 analyzers "A and B" were indicating greater than 4% oxygen concentration. Actual drywell samples revealed the oxygen concentration was 3%. There was no affect on the environs. This was a non-repetitive event. The cause of the occurrence has been attributed to air inleakage to the analyzers causing them to observe a higher than actual reading. The lines were isolated and pressurized, several leaks in the panel were found and repaired. The analyzers were re-calibrated and returned to service. This problem is only applicable to Unit I because the Unit II drywell is. not inerted. The analyzers are not utilized on any other safety related system on either unit.

1592 237 e