ML20067C792: Difference between revisions

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==References:==
==References:==
(a)        J.L. Schrage to T.E. Murley letter dated December 14,1992 (b)    B.L. Siegel to T.J. Kovach letter dated December 23,1992 (c)    P.L. Piet to T.E. Murley letter dated August 20,1993 Mr. Russell, In Reference (a), Commonwealth Edison Company (CECO) submitted a proposed                                                                  :
(a)        J.L. Schrage to T.E. Murley {{letter dated|date=December 14, 1992|text=letter dated December 14,1992}} (b)    B.L. Siegel to T.J. Kovach {{letter dated|date=December 23, 1992|text=letter dated December 23,1992}} (c)    P.L. Piet to T.E. Murley {{letter dated|date=August 20, 1993|text=letter dated August 20,1993}} Mr. Russell, In Reference (a), Commonwealth Edison Company (CECO) submitted a proposed                                                                  :
RWCU Outboard Piping Inspection Plan for Dresden and Quad Cities Stations, in order to.                                                            1 address the requirements of Generic Letter 88-01 (and Supplement 1) with regards to this piping. In Reference (b), the NRC approved the inspection Plan. CECO implemented this Inspection Plan during the twelfth refuel outage on Quad Cities Station Unit 2 (O2R12).
RWCU Outboard Piping Inspection Plan for Dresden and Quad Cities Stations, in order to.                                                            1 address the requirements of Generic Letter 88-01 (and Supplement 1) with regards to this piping. In Reference (b), the NRC approved the inspection Plan. CECO implemented this Inspection Plan during the twelfth refuel outage on Quad Cities Station Unit 2 (O2R12).
                                                                                                                                                               ]
                                                                                                                                                               ]

Latest revision as of 13:33, 31 May 2023

Submits Rev to Proposed Replacement Actions Presented 930820.Rev Proposes to Replace IGSCC Susceptible Outboard Supply & Return Piping & Regenerative Heat Exchangers on Units 1 & 2
ML20067C792
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 02/22/1994
From: Schrage J
COMMONWEALTH EDISON CO.
To: Russell W
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM), Office of Nuclear Reactor Regulation
References
NUDOCS 9403040180
Download: ML20067C792 (3)


Text

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v 1400 Opus Place Downers Grove, liiinois 60515 February 22,1994 Mr. William T. Russell, Director Office of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission Washington D.C.' 20555 Attn.: Document Control Desk

Subject:

Quad Cities Station' Units 1 and 2 Revision to the Reactor Water Cleanup (RWCU) Outboard Piping inspection Plan for Quad Cities Station NRC Docket Nos. 50-254 and 50-265

References:

(a) J.L. Schrage to T.E. Murley letter dated December 14,1992 (b) B.L. Siegel to T.J. Kovach letter dated December 23,1992 (c) P.L. Piet to T.E. Murley letter dated August 20,1993 Mr. Russell, In Reference (a), Commonwealth Edison Company (CECO) submitted a proposed  :

RWCU Outboard Piping Inspection Plan for Dresden and Quad Cities Stations, in order to. 1 address the requirements of Generic Letter 88-01 (and Supplement 1) with regards to this piping. In Reference (b), the NRC approved the inspection Plan. CECO implemented this Inspection Plan during the twelfth refuel outage on Quad Cities Station Unit 2 (O2R12).

]

CECO provided the results of the inspection to the NRC in Reference (c). Based upon the inspection results, CECO also described the proposed RWCU Outboard Piping actions (inspection and replacement) for Quad Cities Station Units 1 and 2 during the upcoming refuel outages. This letter transmits a revision to the proposed replacement actions i previously presented in Reference (c).

. . Current insoection/Reolacement Plan Reference (a) stated that if the total number of supply side indications for a particular unit exceeded 40% of the total number of supply side welds inspected for that unit, CECO would replace the supply side piping (through the regonerative heat exchangers) for that unit during the first refuel outage subsequent to inspections on the i unit (given procurement restraints).

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W.T. Russell February 22,1994 Reference (a) also provided criteria for increased inspections and ultimate replacement actions for the return side piping on a particular unit, subsequent to the initial inspections on that unit. If the initialinspections of the return side welds resulted in flaw indications on a particular unit, CECO would inspect an expanded sample of welds during subsequent outages on that unit. If the totai number of return side indications for a particular unit, with a minimum sample size of eight return side welds, exceeded 40% on that unit, CECO would replace the return sido piping on that unit during the first refuel outage subsequent to the inspections on that unit.

Econosed Insaction/ Replacement Plan CECO proposes to replace all IGSCC susceptible outboard supply and return piping and the regenerative heat exchangers on both Units 1 and 2 with IGSCC resistant material i in lieu of performing any future inspections.

CECO will replace allIGSCC susceptible RWCU outboard supply side piping l (through the regenerative heat exchangers) during the following refuel outages at Quad Cities Station:

02R13 Scheduled to start in January 1995 l

Q1R14 Scheduled to start in September 1995 l l

This proposed replacement schedule is consistent with the original schedule submitted in l Reference (a), in that the RWCU outboard supply side piping will be replaced during the first outage subsequent to inspections on the Unit 2 RWCU outboard piping (Q2R13), and I the first outage subsequent to the originally scheduled inspections for the Unit 1 RWCU outboard piping (Q1R14).

CECO will replace all IGSCC susceptible RWCU outboard return side piping during the following refuel outages at Quad Cities Station:

Q2R14 Scheduled to start in September 1996 Q1R15 Scheduled to start in October 1997 Replacement of the supply side piping prior to the return side piping is consistent with the inspection plan approach submitted in Reference (a), as evidenced by the fact that the inspection plan allows for return side weld inspections during more than one refueling outage prior to necessitating a decision on pipe replacement.

It should also be noted that in conjunction with the replacement of the outboard supply and return piping, the suction and discharge piping for the pumps which had previously been exposed to high tempe'.eture conditions, as discussed in Reference (c),

will also be replaced.

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l

. W.T.' Russell February 22,1994 If there are any further questions, please contact John L. Schrage at 708 663-7283.

Very truly you ,

/ .

/ ),

John- 'chra e Nuc ear Licensing Administrator cc: J. Martin, Regional Administrator-Rill T. Taylor, Senior Resident inspector-Ouad Cities C. Pate!, Project Manager-NRR Office of Nuclear Facility Safety -IDNS l

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