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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M7571999-10-22022 October 1999 Advises That Attachment 1 to ,Marked as Proprietary,Re Safety Limit MCPR & Fuel Vendor Change Will Be Withheld from Public Disclosure Per 10CFR2.790(b)(5) ML20217M2101999-10-19019 October 1999 Forwards NRC Rept Number 17, Requal Tracking Rept from Operator Licensing Tracking Sys.Rept Was Used by NRC to Schedule Requalification Exam for Operators & Record Requal Pass Dates ML20217H8471999-10-18018 October 1999 Discusses Completion of Licensing Action for GL 98-01 & Suppl 1, Yr 2000 Readiness of Computer Sys at Npps, to All Holders of Operating Licenses for NPPs ML20217K8441999-10-15015 October 1999 Submits Revised Commitment to NRC Bulletin 90-01,Suppl 1 for Hope Creek Generating Station ML20217H9771999-10-13013 October 1999 Forwards SRO & RO Initial Exam Rept 50-354/98-302,suppl Rept on 990125-29,mtg Meeting on 990322,990429-30 & 0617-18 in-office Review & 990720 Telcon on Appeal Results.Overall, 11 of 16 Applicants Received NRC Licenses ML18107A5561999-10-0707 October 1999 Requests Relief Associated with Containment Examinations at Hope Creek & Salem Generating Stations.Attachment 1 Includes Proposed Alternatives & Supporting Justification for Relief Requests ML20217C4391999-10-0606 October 1999 Informs That Util Authorized to Administer Initial NRC Retake Written Exam to Applicant Listed,During Week of 991011 ML18107A5501999-10-0505 October 1999 Provides Current Status of Pse&G Actions Re GL 98-01, Y2K Readiness of Computer Sys at Npps, for Salem Nuclear Generating Station,Units 1 & 2 & Hope Creek Nuclear Generating Station ML18107A5521999-10-0505 October 1999 Encourages NRC to Support Abb Combustion Engineering Nuclear Power Request for Priority Review of Generic TR Re Crossflow Ultrasonic Flow Measurement Sys ML20217A9601999-10-0404 October 1999 Forwards Errata Redressing Deficiencies & Correcting Two Typos to Ufsar,Rev 10.Incorporate Attached Pages/Figures Into Controlled Copies of UFSAR ML20217A6861999-10-0101 October 1999 Forwards Insp Rept 50-354/99-05 on 990711-0829.Four Violations Occurred Re Areas of Fire Protection,Operation at Reduced Feedwater Inlet Temp & safety-related Battery Charging Operation & Being Treated as NCVs LR-N990430, Forwards Rev 10 to Hope Creek Generating Station Ufsar,Iaw 10CFR50.71(e).Details Re Each Change Also Attached to Facilitate NRC Review1999-09-28028 September 1999 Forwards Rev 10 to Hope Creek Generating Station Ufsar,Iaw 10CFR50.71(e).Details Re Each Change Also Attached to Facilitate NRC Review ML18107A5341999-09-22022 September 1999 Provides Data Re Operator Licensing Exam for Salem & Hope Creek Station,In Response to NRC Form 536 (7-1999) 05000354/LER-1999-009, Forwards LER 99-009-00, License Condition Violation - Min FW Temp Limits. Commitments Made by Util Encl1999-09-20020 September 1999 Forwards LER 99-009-00, License Condition Violation - Min FW Temp Limits. Commitments Made by Util Encl ML20217K7781999-09-16016 September 1999 Forwards Discharge Monitoring Rept for Hope Creek Generating Station for Month of Aug 1999. Rept Is Required by & Prepared Specifically for EPA & Nj Dept of Environ Protection ML20212B3631999-09-14014 September 1999 Forwards Rev 13 to Salem - Hope Creek Security Plan,Iaw 10CFR50.54(p).Summary of Proposed Changes to Plan,Encl. Encl Withheld ML20212B4021999-09-13013 September 1999 Submits Supplemental Info Related to Hope Creek License Change Request (LCR) H98-08,submitted to NRC on 981230, Re Flood Protection TS Changes ML18107A5221999-09-0808 September 1999 Requests Approval to Use ASME Code Case N546,which Provides Alternative Qualification Requirements That Allow Personnel Most Familiar with Walkdown of Plant Sys,Like License Operators to Perform VT-2 Examinations ML20211N5421999-09-0808 September 1999 Forwards Amend 121 to License NPF-57 & Safety Evaluation. Amend Revises TSs by Relocating Procedural Details of RETS to Offsite Dose Calculation Manual LR-N990395, Provides Comments on NRC Ltr Dtd 990714, Closure of TAC Number MA1194 - Response to RAIs to GL 92-01,Rev 1,Suppl 1, Reactor Vessel Structural Integrity, for Hope Creek Generating Sation. Revised GE Report Encl Also1999-09-0101 September 1999 Provides Comments on NRC Ltr Dtd 990714, Closure of TAC Number MA1194 - Response to RAIs to GL 92-01,Rev 1,Suppl 1, Reactor Vessel Structural Integrity, for Hope Creek Generating Sation. Revised GE Report Encl Also ML18107A4911999-08-20020 August 1999 Forwards Revised Plant Attribute Libraries for Salem & Hope Creek Generating Stations,Iaw 10CFR50,App E,Vi, Emergency Response Data Sys, 3.b.Changes Are Identified by Rev Bars ML20211B5341999-08-20020 August 1999 Forwards RAI Re 2nd 10-yr ISI Interval Relief Requests Re Plant.Info Requested to Be Provided within 60 Days of Receipt of Ltr ML18107A4801999-08-13013 August 1999 Requests That Pse&Gs Contact in NUREG-0383, Directory of Compliance for Radioactive Matl Packages, Be Changed ML20210R4911999-08-11011 August 1999 Forwards Insp Rept 50-354/99-04 on 990530-0711.No Violations Noted.Inspectors Reviewed Performance Indicators Submitted as Part of Pilot Program for New Regulatory Oversight Process & Verified Data ML18107A4751999-08-0505 August 1999 Forwards Fitness for Duty Performance Data Rept for Six Month Period Ending 990630 ML20210H9241999-07-26026 July 1999 Informs That State of Nj Dept of Environ Protection Has No Comments on Licensee 990517 Request for Amend to TS by Adding TS 3.3.10, Instrumentation of OPRM Sys ML20210F3271999-07-22022 July 1999 Forwards SE Granting Relief Requests RR-B1,RR-C1,RR-D1 & RR-B3 Re First 10-year Interval for ISI Program at Hope Creek ML20210D3971999-07-16016 July 1999 Forwards Discharge Monitoring Rept for Hope Creek Generating Station, for June 1999.Rept Is Required by & Prepared for EPA & Nj Dept of Environ Protection ML20209G2831999-07-14014 July 1999 Disclosure Closure of TAC MA1194 Re Licensee Response to RAI to GL 92-01,Rev 1,Suppl 1, Rc Structural Integrity, for Plant 05000354/LER-1999-007, Forwards LER 99-007-00,re License Condition Violation - Class-1E Battery Charging Operation.Commitments Made by Util Encl1999-07-14014 July 1999 Forwards LER 99-007-00,re License Condition Violation - Class-1E Battery Charging Operation.Commitments Made by Util Encl LR-N990250, Provides Proposed Alternative & Supporting Justification for Relief from Augmented Inservice Requirements of 10CFR50.55a(g) for Volumetric Exam of RPV Circumferential Welds1999-07-0909 July 1999 Provides Proposed Alternative & Supporting Justification for Relief from Augmented Inservice Requirements of 10CFR50.55a(g) for Volumetric Exam of RPV Circumferential Welds ML20196J4421999-07-0101 July 1999 Forwards Request for Addl Info Re Increase of Allowable Main Steam Isolation Valve (MSIV) Leak Rate & Deletion of MSIV Sealing Sys for Plant LR-N990316, Responds to NRC Request for Info Re Y2K Readiness at Npps, Per GL 98-01,suppl 1.Disclosure Encl1999-06-30030 June 1999 Responds to NRC Request for Info Re Y2K Readiness at Npps, Per GL 98-01,suppl 1.Disclosure Encl ML18107A4131999-06-25025 June 1999 Provides Further Clarification of Licensing & Design Basis for 125 Vdc Battery Margins for Sgs & HCGS for Meeting Station SBO & Loca/Loop Loading Requirements,Per Util 990426 Ltr & Discussion with NRC ML20209B6441999-06-21021 June 1999 Offers No Comments on Licensee 990529 Request for Revs to Plant Radiological Effluent Ts,Per GL 89-01 ML20209C0621999-06-21021 June 1999 Forwards NPDES Discharge Monitoring Rept,May 1999, for Hcgs.Rept Prepared Specifically for EPA & Nj Dept of Environ Protection ML20196E6471999-06-21021 June 1999 Forwards Revised marked-up TS Page for HCGS License Change Requests H99-02 & H99-05,dtd 990329 & 0524,respectively. Revised Pages Do Not Alter Conclusions Reached in 10CFR50.92 No Significant Hazards Analysis Previously Submitted ML20196F9441999-06-21021 June 1999 Forwards Insp Rept 50-354/99-03 on 990419-0529.Violations Noted.Two Violations of NRC Requirements Occurred Re Reactor Bldg Ventilation Setpoints & Control Rod Drop Analyses ML20212J0541999-06-17017 June 1999 Responds to Requesting That NRC Staff ...Allow BWR Plants Identified to Defer Weld Overlay Exams Until March 2001 or Until Completion of NRC Staff Review & Approval of Proposed Generic Rept,Whichever Comes First ML20196E9631999-06-17017 June 1999 Informs That Util Has Made Change to Commitment Stated in NRC Ser,Suppl 5.Commitment That Has Been Changed Is Item Number 1 of First Paragraph on Page 9-3 of Ser,Suppl 5 LR-N990295, Submits Change 1 to Relief Request RR-A4,which Clarifies Requirements Re Snubber Visual Insps.Request Was Submitted as Part of Plant Second Interval ISI Program on 9905111999-06-16016 June 1999 Submits Change 1 to Relief Request RR-A4,which Clarifies Requirements Re Snubber Visual Insps.Request Was Submitted as Part of Plant Second Interval ISI Program on 990511 05000354/LER-1999-006, Forwards LER 99-006-00 Re Esfa B Channel Primary Containment Isolation Signal Actuation.Attachment a Lists Commitments Util Making to NRC Re LER1999-06-15015 June 1999 Forwards LER 99-006-00 Re Esfa B Channel Primary Containment Isolation Signal Actuation.Attachment a Lists Commitments Util Making to NRC Re LER ML20195J1101999-06-0707 June 1999 Informs of Completion of Review of Providing Updated Status on Implementation of Commitments Made in Response to GL 89-13.Confirms Revs Made to Previous Commitments to Resolve Monitoring Pressure Drop Problem ML20195J1051999-06-0707 June 1999 Informs That NRC Office of Nuclear Reactor Regulation Reorganized Effective 990328.As Part of Reorganization,Div of Licensing Project Mgt Created.Jw Clifford Will Be Section Chief for Hope Creek Generating Station ML20207F2681999-06-0303 June 1999 Responds to by Forwarding Gfes & NRC Written Exam Grades for List of Hope Creek Operators Submitted by DE Jackson.Absence of Gfes Grade Indicates That Operator Previously Issued RO or SRO License.Without Encl ML20207D0201999-05-27027 May 1999 Discusses 990512 Meeting to Identify Insp Activities at Hope Creek Facility Over Next Six Months & Informs of Planned Insps in Order for Licensee to Have Opportunity to Prepare & Provide Region I with Feedback on Schedule Conflicts ML18107A3611999-05-27027 May 1999 Forwards Responses to NRC 990301 & 990323 RAIs for Salem & Hope Creek Generating Stations Relating to GL 96-05 ML20207A3451999-05-20020 May 1999 Discusses Completion of Licensing Action for NRC Bulletin 96-003, Potential Plugging of ECCS Strainers by Debris in Bwrs ML20195B9931999-05-20020 May 1999 Forwards NPDES Discharge Monitoring Rept,Apr 1999, for Hgcs.Rept Prepared Specifically for EPA & Nj Dept of Environ Protection ML20206Q6211999-05-14014 May 1999 Informs That on 990119 Licensee Provided NRC with Several Revised TS Bases Pages for Plant.Ts Bases Pages B 3/4 6-1 & B 3/4 6-2 Were Revised 1999-09-08
[Table view] Category:OUTGOING CORRESPONDENCE
MONTHYEARML20217M7571999-10-22022 October 1999 Advises That Attachment 1 to ,Marked as Proprietary,Re Safety Limit MCPR & Fuel Vendor Change Will Be Withheld from Public Disclosure Per 10CFR2.790(b)(5) ML20217M2101999-10-19019 October 1999 Forwards NRC Rept Number 17, Requal Tracking Rept from Operator Licensing Tracking Sys.Rept Was Used by NRC to Schedule Requalification Exam for Operators & Record Requal Pass Dates ML20217H8471999-10-18018 October 1999 Discusses Completion of Licensing Action for GL 98-01 & Suppl 1, Yr 2000 Readiness of Computer Sys at Npps, to All Holders of Operating Licenses for NPPs ML20217H9771999-10-13013 October 1999 Forwards SRO & RO Initial Exam Rept 50-354/98-302,suppl Rept on 990125-29,mtg Meeting on 990322,990429-30 & 0617-18 in-office Review & 990720 Telcon on Appeal Results.Overall, 11 of 16 Applicants Received NRC Licenses ML20217C4391999-10-0606 October 1999 Informs That Util Authorized to Administer Initial NRC Retake Written Exam to Applicant Listed,During Week of 991011 ML20217A6861999-10-0101 October 1999 Forwards Insp Rept 50-354/99-05 on 990711-0829.Four Violations Occurred Re Areas of Fire Protection,Operation at Reduced Feedwater Inlet Temp & safety-related Battery Charging Operation & Being Treated as NCVs ML20211N5421999-09-0808 September 1999 Forwards Amend 121 to License NPF-57 & Safety Evaluation. Amend Revises TSs by Relocating Procedural Details of RETS to Offsite Dose Calculation Manual ML20211B5341999-08-20020 August 1999 Forwards RAI Re 2nd 10-yr ISI Interval Relief Requests Re Plant.Info Requested to Be Provided within 60 Days of Receipt of Ltr ML20210R4911999-08-11011 August 1999 Forwards Insp Rept 50-354/99-04 on 990530-0711.No Violations Noted.Inspectors Reviewed Performance Indicators Submitted as Part of Pilot Program for New Regulatory Oversight Process & Verified Data ML20210F3271999-07-22022 July 1999 Forwards SE Granting Relief Requests RR-B1,RR-C1,RR-D1 & RR-B3 Re First 10-year Interval for ISI Program at Hope Creek ML20209G2831999-07-14014 July 1999 Disclosure Closure of TAC MA1194 Re Licensee Response to RAI to GL 92-01,Rev 1,Suppl 1, Rc Structural Integrity, for Plant ML20196J4421999-07-0101 July 1999 Forwards Request for Addl Info Re Increase of Allowable Main Steam Isolation Valve (MSIV) Leak Rate & Deletion of MSIV Sealing Sys for Plant ML20196F9441999-06-21021 June 1999 Forwards Insp Rept 50-354/99-03 on 990419-0529.Violations Noted.Two Violations of NRC Requirements Occurred Re Reactor Bldg Ventilation Setpoints & Control Rod Drop Analyses ML20212J0541999-06-17017 June 1999 Responds to Requesting That NRC Staff ...Allow BWR Plants Identified to Defer Weld Overlay Exams Until March 2001 or Until Completion of NRC Staff Review & Approval of Proposed Generic Rept,Whichever Comes First ML20195J1051999-06-0707 June 1999 Informs That NRC Office of Nuclear Reactor Regulation Reorganized Effective 990328.As Part of Reorganization,Div of Licensing Project Mgt Created.Jw Clifford Will Be Section Chief for Hope Creek Generating Station ML20195J1101999-06-0707 June 1999 Informs of Completion of Review of Providing Updated Status on Implementation of Commitments Made in Response to GL 89-13.Confirms Revs Made to Previous Commitments to Resolve Monitoring Pressure Drop Problem ML20207F2681999-06-0303 June 1999 Responds to by Forwarding Gfes & NRC Written Exam Grades for List of Hope Creek Operators Submitted by DE Jackson.Absence of Gfes Grade Indicates That Operator Previously Issued RO or SRO License.Without Encl ML20207D0201999-05-27027 May 1999 Discusses 990512 Meeting to Identify Insp Activities at Hope Creek Facility Over Next Six Months & Informs of Planned Insps in Order for Licensee to Have Opportunity to Prepare & Provide Region I with Feedback on Schedule Conflicts ML20207A3451999-05-20020 May 1999 Discusses Completion of Licensing Action for NRC Bulletin 96-003, Potential Plugging of ECCS Strainers by Debris in Bwrs ML20206Q6211999-05-14014 May 1999 Informs That on 990119 Licensee Provided NRC with Several Revised TS Bases Pages for Plant.Ts Bases Pages B 3/4 6-1 & B 3/4 6-2 Were Revised ML20206Q4461999-05-14014 May 1999 Forwards SE Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant ML20206U8451999-05-14014 May 1999 Forwards Insp Rept 50-354/99-02 on 990308-0418.Violations Re Fuel Handling Errors & Missed Temp Monitoring During Reactor Vessel Head Tensioning Occurred & Being Treated as non-cited Violation ML20206R2691999-05-12012 May 1999 Informs That During 990504 Telcon Between J Caruso & H Hanson,Arrangements Were Made for Administration of Licensing Written Retake Exam at Hope Creek Nuclear Generating Station During Week of 990927 ML20206C8431999-04-22022 April 1999 Forwards SER Authorizing Util 980728 Submitted Relief Requests Associated with Changes Made to Repair Plan for Core Spray Nozzle Weld N5B ML20205S7911999-04-19019 April 1999 Forwards Insp Rept 50-354/99-01 on 990124-0307.Violations Noted.Some Human Performance Errors Occurred During Numerous Outage Activities,Util Appropriately Reacted to Each of Errors & Initiated Corrective Actions ML20205R0461999-04-14014 April 1999 Forwards Associated Page with Correction Marked in Margin of PPR of Salem Issued 990409.During Final Review of Hard Copy, Error Was Noted.Without Encl ML20205R0861999-04-14014 April 1999 Informs That Final Review of Hard Copy of PPR Re Hope Creek, Issued 990409 Had Error.Electronic Version e-mailed Was Not Effected.Forwards Pp with Correction in Margin.Without Encl ML20205N2111999-04-0909 April 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-354/98-302 Issued on 990226.Response Indicates That Licensee Corrected Violation & Initiated Measures to Prevent Recurrence ML20205N2481999-04-0909 April 1999 Discusses Hope Creek Generating Station Plant Performance Review Conducted for Period April 1998 Through Jan 1999 & Informs of NRC Planned Insp Effort Resulting from Ppr. Historial Listing & Insp Plans for Next Few Months Encl ML20205G5961999-03-19019 March 1999 Forwards Safety Evaluation of Relief Request Re ASME Code Case N-567, Alternate Requirements for Class 1,2 & 3 Replacement Components Section Xi,Div 1. Request Acceptable ML20205F8771999-03-18018 March 1999 Forwards SE Authorizing Licensee 971222 Relief Requests Re Second 10-year Interval for Pumps & Valves IST Program for Hope Creek Generating Station ML20207D5741999-03-0101 March 1999 Discusses Pse&G 980604 Updated Response to GL 96-05 Indicating Intent to Implement Provisions of JOG Program on MOV Periodic Verification at Hope Creek Generating Station. Forwards RAI Re GL 96-05 Program at Hope Creek ML20198H6211998-12-24024 December 1998 Forwards Notice of Withdrawal of 970826,as Suppl 980424 & 0924 Amend Request for FOL NPF-57.Proposed Change Would Have Modified Facility TSs Pertaining to Filtration,Recirculation & Ventilation Sys Surveillance Testing Requirements ML20198L3571998-12-22022 December 1998 Forwards Insp Rept 50-354/98-11 on 981101-1212.No Violations Noted.Insp Generally Characterized by safety-conscious Operations,Effective Engineering & Maint Practices & Careful Radiological Work Controls ML20198H6661998-12-17017 December 1998 Informs That Attachment 1 to Ltr LR-N98404,dtd 980825 Marked as Proprietary,Will Be Withheld from Public Disclosure Pursuant to 10CFR2.790(b)(5) & Section 103(b) of Atomic Energy Act of 1954,as Amended ML20196K1371998-12-0909 December 1998 Advises of Planned Insp Effort Resulting from Hope Creek Insp Review Planning Meeting Conducted on 981110.Details of Insp Plan for Next 6 Months Encl ML20197H3841998-12-0707 December 1998 Informs That Licensee Authorized to Administer Initial Written Exams to Listed Applicants on 981222.NRC Region I Operator Licensing Staff Will Administer Operating Tests ML20196H0301998-12-0101 December 1998 Informs That NEDC-32511P,rev 1,dtd Oct 1998 Marked as Proprietary,Will Be Withheld from Public Disclosure Pursuant to 10CFR2.790(b)(5) & Section 103(b) of Atomic Energy Act of 1954,as Amended ML20196F7991998-11-30030 November 1998 Forwards Rept Representing Results of 981026-29 Audit of Year 2000 Pragram at Hope Creek Generating Station.Audit Conducted as Followup to NRC GL 98-01, Year 2000 Readiness of Computer Sys at Npps, Issued 980511 ML20196D0711998-11-23023 November 1998 Forwards Insp Rept 50-354/98-10 on 980920-1031 & Notice of Violation Re Preforming Single Cell Charge on safety-related Battery Cell in Configuration Prohibited by Station Procedures ML20154Q7071998-10-16016 October 1998 Forwards Exam Rept 50-354/98-03OL Conducted by NRC During Periods of 980304-12,0519-21,22-28 & 0629.All Five Reactor Operator Applicants & Four of Five Senior Reactor Applicants Passed Exams IA-98-323, First Final Response to FOIA Request for Records.Records in App a Available in Pdr.Records in App B Partially Withheld (Ref FOIA Exemption 3)1998-10-0909 October 1998 First Final Response to FOIA Request for Records.Records in App a Available in Pdr.Records in App B Partially Withheld (Ref FOIA Exemption 3) ML20154J8501998-10-0909 October 1998 Forwards Insp Rept 50-354/98-08 on 980809-0919 & Notice of Violation Re Inadequate Corrective Actions to Resolve Steam Leaks from Piping Located in Torus Room ML20154P4011998-10-0909 October 1998 First Final Response to FOIA Request for Records.Records in App a Available in Pdr.Records in App B Partially Withheld (Ref FOIA Exemption 3) ML20154F1121998-10-0202 October 1998 Forwards Insp Rept 50-354/98-09 on 980817-26 & 0908.No Violations Identified.Major Areas Inspected:Maint, Engineering & Mgt Meeting ML20154B3341998-09-29029 September 1998 Requests That Encl Info on GE Rept NEDC-32511P Be Reviewed & Revised Proprietary Version of Subj Rept Be Submitted.Some Info in Rept Should Not Be Exempt from Public Disclosure & Should Be Released & Placed in PDR ML20154B3781998-09-25025 September 1998 Informs That Facility Scheduled to Administer NRC Generic Fundamentals Exam on 981007.Sonalysts,Inc Authorized Under Contract to Support NRC in Administration of Activities. Ltr & Encls Provide Instructions & Guidelines ML20151Z1111998-09-11011 September 1998 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-354/98-06 Issued on 980721 ML20151Z5941998-09-11011 September 1998 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-354/98-02 on 980423.Response Indicated Violations Corrected & Measures Initiated to Prevent Recurrence ML20151W9711998-09-10010 September 1998 Informs That as Part of NRC PRA Implementation Plan, Commission Has Assigned Two Senior Reactor Analysts (Sras) to Each Regional Ofc.T Shedlosky & J Trapp Have Been Assigned as SRAs in Region I 1999-09-08
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April 16,1998 Mr. Harold Executive Vice President Nuclear Business Unit Public Service Electric & Gas Company PO Box 236 Hancocks Bridge, NJ 08038 SUBJECT: Inspection Report 50-354/97-10
Dear Mr. Keiser:
This letter refers to your March 4,1998, correspondence (LR-N98074,in response to in our February 3,1998 letter regarding the Hope Creek facility.
Thank you for informing us of the corrective and preventive actions for the Notice of Violation, as documented in your letter. The violation included failures to appropriately establish or implement three technical specification required maintenance procedures, a failure to provide sufficient instructions for installing a reactor water cleanup system flow element, and a failure to implement adequate corrective actions to prevent a repeat reactor core isolation cooling system governor valve malfunction. We noted that you have largely completed your corrective actions in response to this Notice of Violation, and have ascribed the cause of many of the noted issues to personnel error. We will review the effectiveness of your actions in a future inspection.
Your cooperation with us is appreciateo.
Sincerely, Original Signed By:
James C. Linville, Chief Projects Branch 3 Division of Reactor Projects
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Docket No. 50-354 l l 9804210060 980416 PDR ADOCK 05000354 s '. hl G PDR lV L_
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Mr. Harold cc:
L. Storz, Senior Vice President - Nuclear Operations E. Simpson, Senior Vice President - Edear Engineering E. Salowitz, Director - Nuclear Business Support M. Bezilla, General Manager - Hope Creek Operations J. McMahon, Director - QA/ Nuclear Training / Emergency Preparedness D. Powell, Manager - Licensing and Regulation A. C. Tapert, Program Administrator cc w/cy of Licensee's Letter:
A. F. Kirby, Ill, External Operations - Nuclear, Delmarva Power & Light Co.
J. A. Isabella, Manager, Joint Generation Atlantic Electric R. Kankus, Joint Owner Affairs Jeffrey J. Keenan, Esquire M. J. Wetterhahn, Esquire Consumer Advocate, Office of Consumer Advocate q William Conklin, Public Safety Consultant, Lower Alloways Creek Township State of New Jersey State of Delaware i
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Mr. Harold Distribution w/ copy of Licensee's Response Letter:
Region I Docket Room (with concurrences)
Nuclear Safety information Center (NSIC)
NRC Resident inspector PUBLIC D. Screnci, PAO J. Linville, DRP S. Barber, DRP C. O'Daniell, DRP B. McCabe, OEDO J. Stolz, PD1-2, NRR R. Ennis, Project Manager (Acting), NRR R. Correia, NRR F. Talbot, NRR inspection Program Branch, NRR (IPAS)
DOCDESK DOCUMENT NAME: G:\ BRANCH 3\REPLYLTR\9710 RESP.HC Ts receive a copy of this document. Indicate in the box: "C" = Copy without attachment / enclosure "E" = Copy with attachment / enclosure *N*=
No copy OFFICE Rl/DRP ,, / /
NAME JLinvi}tt()to g dL DATE 04/15/98 04/ /98 04/ /98 04/ /98 04/ /98 OFFICIAL RECORD COPY
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Public Se'vice Eiocine ano Gas Comneny Louis F. Stor Public Sennce Electnc and Ges Company P.O. Box 236, Mancocks Bridge, NJ 08038 609-339 5700
$wo victPmew.NuewOpronons
United States Nuclear Regulatory Commission l Document Control Desk . i Washington, DC 20555 l
REPLY TO NOTICE OF VIOLATION INSPECTION REPORT NO. 50-354/97-10 NOPE CREEK GENERATING STATION 4 FACILITY OPERATING LICENSE NPF-57 I DOCKET NO. 50-354 l l
Gentlemen: l Pursuant to the provisions of 10CFR2.201, Public Service Electric and Gas Company (PSE&G) hereby submits replies to the Notices of violation (NOV) issued to the Hope Creek Generating Station in a
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letter dated February 3, 1998. The violations contained in l Appendix A of the February 3rd letter concerned: 1) three '
examples of a failure to properly establish or implement procedures, as required by Technical Specification 6.8.1.a, 7- s during maintenance activities; 2) a failure to properly establish i
instructions, procedures or drawings for the correct orientation of a reactor water cleanuo system flow measurement orifice plate, as required by 10CFR50, Appendix B, Criterion V; and 3) a failure t'o implement effective corrective actions to preclude recurrence of a Reactor Core Isolation Cooling system governor valve
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malfunction, as required by 10CFR50, Appendix B, Criterion XVI.
The concerns related to personnel performance and supervisory oversight noted in the inspection report will continue to be addressed by PSE&G. In addition to the corrective actions taken/ planned for the specific performance issues and procedure deficiencies, PSE&G is taking measures to comprehensively address human performance in the Maintenance Department. Specifically, PSE&G is planning to implement " lessons learned" roll outs from the Maintenance Department intervention on an approximate quarterly basis. These roll outs will focus on and reinforce management expectations, cultural behaviors, human performance and corrective actions from significant conditions adverse to
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quality. As recaired, personnel performance will continue to be assessed on an individual basis and corrective actions taken when
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appropriate.
To address repetitive personnel performance issues, including inadequate Technical Specification procedure revisions, PSE&G l '/ will continue to utilize the corrective action program to:
resolve specific conditions adverse te quality; 2) identify 1)
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O rnnwon Yif'0 l000) % lUff
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IAAR 041998 i
'p Document Control Desk LR-N98074-2- {
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significant trends in departmental and station performance; and 3) implement corrective measures to improve overall station operatien. This process was used to resolve the conditions adverse to quality identified in the inspection report's Notice of Violation as described in PSE&G's associated response i (Attachment 1) . l Shouldyouhaveanyquestionsorcommentsont$listransmittal,do l l
not hesitate to contact us. i l
Sincerely, V -
f~)eud ,
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Attachment (1)
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.g gpR 0 41998 Document Control Desk -3-LR-N98074 I
C Mr. H. Miller, Administrator - Region I U. S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 Ms. B. Mozafari, Licensing Project Manager - HC U. S. Nuclear Regulatory Commission One White Flint North 11555 Rockville Pike Mail Stop 14E21 Rockville, MD 20852 Mr. D. Jaffe, Licensing Project Manager - HC (Acting)
U. S. Nuclear Regulatory Commission One White Flint North 11555 Rockville Pike i Mail Stop 14E21 Rockville, MD 20852
Mr. S. Morris (X24)
USNRC Senior Resident Inspector - HC b Mr. K. Tosch, Manager IV Bureau of Nuclear Engineering P. O. Box 415 Trenton, NJ 08625
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/ Attachment 1 LR-N98074 RESPONSE TO NOTICE OF VIOLATION INSPECTION REPORT NO. 50-354/97-07 HOPE CREEK GENERATING STATION DOCKET NO. 50-354
!. REPLY TO THE NOTICE OF VIOLATION A. Technical Specification 6.8.1 Violation *
1. DescriDtion of the Notice of Violation
" Hope Creek technical specification (TS) 6.8.1 requires, in
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part, that written procedures shall be established, implemented and maintained for applicable activities specified in Appendix A of Regulatory Guide (RG) 1.33, Revision 2. TS 6.8.1 also requires that written procedures shall be established for surveillance and test activities of safety-related equipment.
Appendix A of RG 1.33 requires that procedures be established for startup, operation, and' shutdown of the Reactor Core Isolation Cooling (RCIC) system, as well as for the cca. trol of maintenance, repair or replacement of components tu_. can
,_, affect the performance of safety-related equipment.
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Contrary to the above, three examples of failures to either establish or implement the above required procedures were identified:
a. On November 24, 1997, maintenance technicians failed to follow Hope Creek procedure HC. IC-DC.ZZ-0140 (Q) ,
Revision 3, " Device / Equipment Calibration Masoneilan Pressure and Temperature Controllers," in that they did not restore a gain adjustment in the "B" control room ventilation system chiller pressure control valve circuitry to the proper value following an instrument calibration. This led to two subsequent trips of the safety-related chiller due to high back pressure.
b. On December 30, 1997, it was identified that procedure HC.OP-SO.BD-0001(Q), Revision 16, " Operation of the Reactor Core Isolation Cooling System," failed to provide adequate guidance for resetting the turbine mechanical overspeed trip device. As a result, the RCIC turbine trip throttle valve could not be re-opened for several hours following system maintenance, c. On January 3, 1998, it was identified that maintenance s department procedure HC.MD-ST.SB-0006 (Q) , Revision 0, Page 1 of 7 i
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mar-% ear upes FM l',, * Attachment 1 LR-N98074
- g e's "18 Month Electrical Protection Assembly Channel l Calibration," established in part to implement the surveillance test requirements of TS 4.8.4.6.b, did not incorporate the appropriate acceptance criteria for
- under-frequency channel calibrations. Specifically, step 5.9.8 of the noted procedure lists the acceptance criteria as "57 Hertz," while the associated TS specifies the criteria as "57 Hertz, -0% + 2%."
l These are Severity Level IV violations (Supplement I).
2. Reply to Notice of Violation PSE&G agrees with the above three violations.
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3. Reason for the Violation v'iolation a. f PSE&G has attributed the cause of procedure non-compliance to personnel error. Due to an inadequate review of personnel qualification, a maintenance supervisor inappropriately assigned a non-qualified technician to perform pneumatic controller adjustments, and as a result, the procedure was l not properly completed. Contributing to the procedure non- l compliance was the lack of a questioning attitude and failure
/" of the technician to notify supervision of procedure steps that he could not complete as required.
Violation b.
PSE&G has attributed the cause of the failure to provide appropriate guidance for resetting the turbine mechanical overspeed trip device to over reliance on the " skill of the craft" to reset a RCIC overspeed trip. Successful resetting of RCIC overspeed trips during previous 18 month surveillances did not provide an opportunity to identify a need to provide additional procedural guidance on ensuring proper seating of the RCIC trip tappet assembly. In addition, PSE&G notes that the time to reset the RCIC overspeed trip was the result of planning controlled investigations of the overspeed trip.
Violation c.
PSE&G has attributed the cause of the improper development of the electrical protection assembly calibration procedure to personnel error. Although the new calibration procedure provided appropriate guidance for setting the frequency trJp setpoint, a less than adequate review of TS requirements by the procedure writer and subsequent reviewers resulted in es-l ( left and as-found ac:eptance criteria in the calibration procedure that did not correspond to the TS acceptance criteria.
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m VQur
., AttOchment 1 LR-N98074 yr's
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4. Corrective Steos That Have Been Taken and Results Achieved Violation a.
a. The ventilation train chiller pneumatic controller was properly reset and the chiller was successfully placed in service on November 24, 1997.
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b. The Maintenance personnel involved were held accountable for their actions in accordance with PSE&G's disciplinary policy.
Violation b.
a. The RCIC operating procedure was revised to add steps that ensure the trip tappet assembly is properly seated during a reset of an overspeed trip.
Violation c.
l a. The Maintenance personnel involved were held accountable for his actions in accordance with PSE&G's disciplinary policy.
b. Similar procedure sections covering undervoltage and
/"% overvoltage testing (ir procedures HC.MD-ST.SB-0004 & -
0006) were reviewed to ensure that TS acceptance criteria were properly implemented. No other deficiencies were identified.
c. Maintenance procedure HC.MD-ST.SB-0006 was revis'ed to provide acceptance criteria that appropriately reflects the TS requirements. l 5. Corrective S_ tees That Will Be_Taken to Avoid Further !
Violations I violation a.
No additional corrective actions are planned.
Violation b.
No additional corrective actions are planned.
Violation c.
a. A review of other recently revised or created maintenance surveillance procedures will take place to
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' ensure thet TS acceptance criteria are being appropriately implemented. These activities will be completed by May 30, 1998.
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,, * Attachment 1 LR-N98074 6. Date When Full Comoliance Will Be Achieved Violation a.
Full compliance was achieved on November 24, 1997, when qualified personnel properly set the pneumatic controller for the. ventilation train and the associated chiller unit was placed successfully in service.
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Violation b.
Full compliance was achieved on December 31, 1997, when the RCIC operating procedure was revised to provide additional guidance on resetting of an overspeed trip.
Violation c.
Full compliance was achieved February 25, 1998, when maintenance procedure HC.MD-ST.SB-0006 was revised to reflect the appropriate 18 month TS surveillance teot requirements.
B. 10 CFR 50, Appendix B, Criterion V Violation 1. Descriotion of the Notice of Violation g- s "10 CFR 50, Appendix B, Criterion V, requires in part that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings,and shall be accomplished in accordance with these instructions, procedure or drawings.
Contrary to the above, on November 29, 1997, it was identified that no instruction, procedure, or drawing was provided to workers regarding the correct orientation of a reactor water cleanup system LRWCU) flow measurement orifice during system maintenance. Specifically, while restoring from a corrective maintenance activity to repair an associated RWCU piping flange leak, technicians installed the noted orifice plate backwards in part because no specific guidance for proper reassembly was provided. The orifice plate provides a flow signal to primary containment isolation logic."
This is a Severity Level IV violation (supplement I).
2. Reolv to Notice of Violation PSE&G ngrees with the violation.
3. Reason for the violation O
PSE&G has attributed the cause of the failure to provide i
appropriate guidance for the re-installation of the RWCU flow Page 4 of 7
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e fr.@@ 1 i
,, * Attnchment 1 -
LR-N98074 l l
yr s orifice to reliance on the " skill of the craft" of the '
! maintenance personnel. Flow orifice elements are normally marked to provide indication to maintenance personnel on their proper orientation during reassembly. However, the RWCU flow orifice, installed during plant construction, was not marked to indicate its proper orientation. Due to this lack of orientation indication and a lack of a questioning attitude on the part of a maintenance worker performing this task, the RWCU flow orifice was not installed in the correct orientation. .
4. Corrective Steos That Have Been Taken and Results Achieved a. An evaluation has been completed to confirm the i'
operability of the flow orifice in the installed orientation.
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5. Corrective Steos That Will_Be_Taken to Avoid Further Violations a. A work order will be created to ensure that orientation indication is provided on the RWCU flow orifice element during the next RWCU flow orifice removal and re-installation. The work order will be created by
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September 30, 1998. 1 O b. Lessons learned from this event with respect to questioning proper component configuration will be
!
I rolled out to Maintenance Department personnel. This will be completed by May 5, 1998.
6. Date When Full Compliance Will Be Achieved With the completed evaluation confirming the operability of the flow orifice in the installed orientation on November 29, 1997, full compliance was achieved.
C. 10 CFR 50, Appendix B, Criterion XVI Violation l 1. pgscriotion of the Notice _of Violation
"10 CPR 50, Appendix B, Criterion XVI, requires in part that for significant conditions adverse to quality such as failures, malfunctions, and deficiencies, measures shall be established to assure that the cause of the condition is determined and corrective actions are taken to preclude repetition.
Contrary to the above, prior to December 5, 1997, corrective measures implemented subsequent to a December 28, 1996
[' failure of the RCIC turbine governor valve assembly were insufficient to preclude recurrence. Specifically, the
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Page 5 of 7
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Attachment 1 LR-N98074
.p f
governor valve stem was replaced following the 1996 event with a material design that exhibits an increased thermal expansion rate as material temperature increases. The engineering analysis which supported the stem material change did not account for this factor, and led to governor valve stem binding and a RCIC system failure on December 5, 1997.'
This is a Severity Level IV violation (Supplement I) . }
2. Reply to Notice of Violation ,
.
i PSE&G agrees with the violation.
3. Reason for..the violation j
PSE&G has attributed the cause for the December 5, 1997 RCIC system failure to personnel error. In March 1997, as a I result of increasing occurrences of governor control valve stem binding due to galvanic corrosion, the Nitrided 410 Stainless Steel stem was replaced with a stem manufactured from Inconel 718. Although the Engineering personnel involved in the equivalent replacement part evaluation of the Inconel stem reviewed the material suitability to address the industry concerns with corrosion induced binding, the evaluation failed to appropriately address the difference in thermal exptnsion coefficients between the original nitrided stainless steel shaft and the Inconel shaft. In addition, the evaluation failed to identify that the replacement shaft had a wider manufacturing tolerance (0.4985" to 0.499" for the original, 0.498" to 0.500" for the replacement) since the proprietary shaft dimensions for the original shaft were not available. Since the replacement Inconel stem was purchased to a BW/IP drawing with dimensional specifications consistent to those successfully tested and placed in sertice at other utilities, the Engineering personnel did not fully evaluate the effects of thermal expansion. As a result, the change in dimension coupled with the greater thermal expansion coefficient caused binding of the shaft at elevated RCIC operating temperatures.
4. Corrective Steps That Have Been Taken and Results Achieved a. An appropriate carbon spacer inner diameter was calculated to account for thermal expansion of the replacement Inconel stem. The carbon spacers were re-sized prior to reassembly of the RCIC turbine governor valve and the RCIC system was successfully tested and placed into service.
b. Hope Creek Maintenance Procedure HC.MD-CM.FC-0002 (Q),
/"5 " Reactor Core Isolation Cooling (RCIC) Turbine Steam Stop and Governor Valve Overhaul", was revised to clarify the requirements associated with assuring Page 6 of 7 l
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, * Attachment 1 LR-N98074
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adequate clearance between the valve stem and carbon fs spacers.
5. Corrective Steps That Will Be Taken to Avoid Further violatieng a. Lessons learned from this event will be rolled out to Engineering personnel conducting equivalent replacement evaluations by April 30, 1998, b. Purchase specifications / drawings for the RCIC governor valve stem will be revised to accommodate increased thermal expansion of Inconel 718 versus 410 Stainless Steel by April 30, 1998.
6. Date When Full Comoliance Will Be Achieved Hope Creek is in full compliance. With the successful implementation of corrective actions to resolve the RCIC
, governor valve stem binding, the RCIC system has been restored to an operable condition.
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Page 7 of 7
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TOTAL P.11